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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION  
{{#Wiki_filter:UNITED STATES  
REGION I 475 ALLENDALE ROAD KING OF PRUSSIA, PA 19406-1415  
NUCLEAR REGULATORY COMMISSION  
March 17, 2008
REGION I  
 
475 ALLENDALE ROAD  
KING OF PRUSSIA, PA 19406-1415  
   
   
March 17, 2008
   
   
   
   
Mr. Britt T. McKinney Senior Vice President and Chief Nuclear Officer  
Mr. Britt T. McKinney  
Senior Vice President and Chief Nuclear Officer  
PPL Susquehanna, LLC  
PPL Susquehanna, LLC  
769 Salem Blvd. - NUCSB3  
769 Salem Blvd. - NUCSB3  
Berwick, PA 18603-0467  
Berwick, PA 18603-0467  
 
SUBJECT: SUSQUEHANNA STEAM ELECTRIC STATION, UNITS 1 AND 2 PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION  
SUBJECT:  
SUSQUEHANNA STEAM ELECTRIC STATION, UNITS 1 AND 2  
PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION  
INSPECTION REPORTS NOS. 05000387/2008006; 05000388/2008006  
INSPECTION REPORTS NOS. 05000387/2008006; 05000388/2008006  
   
   
Dear Mr. McKinney:  
Dear Mr. McKinney:  
  On February 1, 2008, the US Nuclear Regulatory Commission (NRC) completed a team  
   
On February 1, 2008, the US Nuclear Regulatory Commission (NRC) completed a team  
inspection at the Susquehanna Steam Electric Station.  The enclosed inspection report  
inspection at the Susquehanna Steam Electric Station.  The enclosed inspection report  
documents the inspection results, which were discussed on February 1, 2008, with you and  
documents the inspection results, which were discussed on February 1, 2008, with you and  
members of your staff.  
members of your staff.  
 
This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, and compliance with the Commission
This inspection was an examination of activities conducted under your license as they relate to  
=s rules and regulations and the conditions of your license.  Within these areas, the inspection involved examination of selected procedures and representative records, observations of activities, and interviews with personnel.  
the identification and resolution of problems, and compliance with the Commission=s rules and  
 
regulations and the conditions of your license.  Within these areas, the inspection involved  
examination of selected procedures and representative records, observations of activities, and  
interviews with personnel.  
   
   
On the basis of the sample selected for review, the team concluded that the implementation of  
On the basis of the sample selected for review, the team concluded that the implementation of  
the corrective action program (CAP) was adequate in that personnel identified issues at a low threshold; generally screened and prioritized issues in a timely manner; evaluated the issues commensurate with their safety significance; and implemented corrective actions in a timely manner commensurate with the safety significance.   
the corrective action program (CAP) was adequate in that personnel identified issues at a low  
 
threshold; generally screened and prioritized issues in a timely manner; evaluated the issues  
commensurate with their safety significance; and implemented corrective actions in a timely  
manner commensurate with the safety significance.   
   
   
The team identified four findings of very low safety significance (Green).  These findings were determined to involve violations of regulatory requirements.  However, because each of the violations was of very low safety significance (Green) and because they were entered into your corrective action program, the NRC is treating these as Non-Cited Violations (NCVs), in accordance with Section VI.A.1 of the NRC
The team identified four findings of very low safety significance (Green).  These findings were  
=s Enforcement Policy.  If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report,  
determined to involve violations of regulatory requirements.  However, because each of the  
violations was of very low safety significance (Green) and because they were entered into your  
corrective action program, the NRC is treating these as Non-Cited Violations (NCVs), in  
accordance with Section VI.A.1 of the NRC=s Enforcement Policy.  If you contest any NCV in  
this report, you should provide a response within 30 days of the date of this inspection report,  
with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:  Document  
with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN:  Document  
Control Desk, Washington DC, 20555-0001, with copies to the Regional Administrator, Region I;
Control Desk, Washington DC, 20555-0001, with copies to the Regional Administrator, Region I;  
 
B. McKinney  
B. McKinney  
  2the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC, 20555-0001; and the NRC Resident Inspector at the Susquehanna facility.  
   
  In accordance with 10 CFR 2.390 of the NRC
2
=s A Rules of Practice,@ a copy of this letter and its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the  
the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC,  
NRC=s document system (ADAMS).  ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
20555-0001; and the NRC Resident Inspector at the Susquehanna facility.  
  Sincerely,  /RA/  Mel Gray, Chief Technical Support & Assessment Branch  
   
In accordance with 10 CFR 2.390 of the NRC=s ARules of Practice,@ a copy of this letter and its  
enclosure, and your response (if any), will be available electronically for public inspection in the  
NRC Public Document Room or from the Publicly Available Records (PARS) component of the  
NRC=s document system (ADAMS).  ADAMS is accessible from the NRC Web site at  
http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).  
   
Sincerely,  
   
/RA/  
   
Mel Gray, Chief  
Technical Support & Assessment Branch  
Division of Reactor Projects  
Division of Reactor Projects  
   
   
Docket Nos.  50-387, 50-388  
Docket Nos.  50-387, 50-388  
License Nos.  NPF-14; NPF-22  
License Nos.  NPF-14; NPF-22  
Enclosure:  Inspection Report Nos. 05000387/2008006; 05000388/2008006    w/ Attachment:  Supplemental Information
   
   
cc w/encl:   
Enclosure: 
Inspection Report Nos. 05000387/2008006; 05000388/2008006
  w/ Attachment:  Supplemental Information
cc w/encl:  
   
C. Gannon, Vice President, Nuclear Operations   
C. Gannon, Vice President, Nuclear Operations   
R. Paley, General Manager, Plant Support R. Pagodin, General Manager, Nuclear Engineering   
R. Paley, General Manager, Plant Support  
 
R. Pagodin, General Manager, Nuclear Engineering   
R. Sgarro, Manager, Nuclear Regulatory Affairs  
R. Sgarro, Manager, Nuclear Regulatory Affairs  
Supervisor, Nuclear Regulatory Affairs  
Supervisor, Nuclear Regulatory Affairs  
 
M. Crowthers, Supervising Engineer, Nuclear Regulatory Affairs  
M. Crowthers, Supervising Engineer, Nuclear Regulatory Affairs R. Peal, Mgr, Training, Susquehanna  
R. Peal, Mgr, Training, Susquehanna  
Manager, Quality Assurance  
Manager, Quality Assurance  
J. Scopelliti, Community Relations Manager, Susquehanna   
J. Scopelliti, Community Relations Manager, Susquehanna   
B. Snapp, Esq., Associate General Counsel, PPL Services Corporation  
B. Snapp, Esq., Associate General Counsel, PPL Services Corporation  
Supervisor - Document Control Services  
Supervisor - Document Control Services  
R. Osborne, Allegheny Electric Cooperative, Inc. D. Allard, Dir, PA Dept of Environmental Protection   
R. Osborne, Allegheny Electric Cooperative, Inc.  
D. Allard, Dir, PA Dept of Environmental Protection   
Board of Supervisors, Salem Township  
Board of Supervisors, Salem Township  
J. Johnsrud, National Energy Committee, Sierra Club  
J. Johnsrud, National Energy Committee, Sierra Club  
E. Epstein, TMI-Alert (TMIA)  
E. Epstein, TMI-Alert (TMIA)  
J. Powers, Dir, PA Office of Homeland Security
R. French, Dir, PA Emergency Management Agency


J. Powers, Dir, PA Office of Homeland Security R. French, Dir, PA Emergency Management Agency
 
  Enclosure
1 U.S. NUCLEAR REGULATORY COMMISSION
   
   
REGION I
  Docket No: 50-387, 50-388
   
   
   
   
License No: NPF-14, NPF-22  
Enclosure
 
  Report No: 05000387/2008006, 05000388/2008006  
1
 
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket No:
50-387, 50-388
License No:  
NPF-14, NPF-22  
Report No:  
05000387/2008006, 05000388/2008006  
Licensee:
PPL Susquehanna, LLC
Facility:
Susquehanna Steam Electric Station, Units 1 and 2
Location:
769 Salem Boulevard - NUCSB3
Berwick, PA  18603-0467
Dates:
January 14 - February 1, 2008
Team Leader:
B. Norris, Senior Project Engineer, Division of Reactor Projects
Inspectors:
F. Arner, Senior Reactor Inspector, Division of Reactor Safety
R. Fuhrmeister, Senior Project Engineer, Division of Reactor Projects
G. Ottenberg, Resident Inspector, Division of Reactor Projects
J. Bream, Reactor Engineer, Division of Reactor Projects
R. McKinley, Operations Examiner, Division of Reactor Safety
   
   
   
   
Licensee: PPL Susquehanna, LLC
Approved by:  
 
Mel Gray, Chief
  Facility: Susquehanna Steam Electric Station, Units 1 and 2
 
   
   
Technical Support & Assessment Branch
   
   
Location: 769 Salem Boulevard - NUCSB3  Berwick, PA  18603-0467
Division of Reactor Projects
   
   
   
   
Dates: January 14 - February 1, 2008
  Team Leader: B. Norris, Senior Project Engineer, Division of Reactor Projects


   
   
   
   
Inspectors: F. Arner, Senior Reactor Inspector, Division of Reactor Safety
R. Fuhrmeister, Senior Project Engineer, Division of Reactor Projects  G. Ottenberg, Resident Inspector, Division of Reactor Projects  J. Bream, Reactor Engineer, Division of Reactor Projects
R. McKinley, Operations Examiner, Division of Reactor Safety
   
   
  Approved by: Mel Gray, Chief  Technical Support & Assessment Branch
Enclosure
Division of Reactor Projects
   
 
2
SUMMARY OF FINDINGS
   
   
 
IR 05000387/2008-006, 05000388/2008-006; 01/14/2008 - 02/01/2008; Susquehanna Steam  
  Enclosure
Electric Station; Biennial Baseline Inspection of the Identification and Resolution of Problems;  
2SUMMARY OF FINDINGS
Corrective Action Program, Simulator Fidelity, and Procedure Quality.  
  IR 05000387/2008-006, 05000388/2008-006; 01/14/2008 - 02/01/2008; Susquehanna Steam Electric Station; Biennial Baseline Inspection of the Identification and Resolution of Problems; Corrective Action Program, Simulator Fidelity, and Procedure Quality.  
 
   
   
This team inspection was performed by five NRC regional inspectors and one resident  
This team inspection was performed by five NRC regional inspectors and one resident  
inspector.  Four findings of very low safety significance (Green) were identified during this inspection and determined to be Non-Cited Violations (NCVs).  The significance of most findings is indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter (IMC) 0609, ASignificance Determination Process
inspector.  Four findings of very low safety significance (Green) were identified during this  
@ (SDP).  The NRC
inspection and determined to be Non-Cited Violations (NCVs).  The significance of most findings  
=s program for overseeing  
is indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter  
the safe operation of commercial nuclear power reactors is described in NUREG-1649, A Reactor Oversight Process,@ Revision 4, dated December 2006.  
(IMC) 0609, ASignificance Determination Process@ (SDP).  The NRC=s program for overseeing  
the safe operation of commercial nuclear power reactors is described in NUREG-1649, AReactor
Oversight Process,@ Revision 4, dated December 2006.  
Identification and Resolution of Problems
   
   
Identification and Resolution of Problems
 
The team concluded that the implementation of the corrective action program (CAP) at  
The team concluded that the implementation of the corrective action program (CAP) at  
Susquehanna was adequate in that personnel identified issues at a low threshold and used a single entry-point system to document the problems by the initiation of an Action Request (AR). About 20 percent of the ARs were considered to be conditions adverse to quality (CAQ) and  
Susquehanna was adequate in that personnel identified issues at a low threshold and used a  
single entry-point system to document the problems by the initiation of an Action Request (AR).  
About 20 percent of the ARs were considered to be conditions adverse to quality (CAQ) and  
sub-classified as a Condition Report (CR).  However, the team identified several ARs that  
sub-classified as a Condition Report (CR).  However, the team identified several ARs that  
should have been classified as CAQs; as a result, CRs were not written and corrective actions  
should have been classified as CAQs; as a result, CRs were not written and corrective actions  
were not timely.  The team identified two findings of very low significance related to the AR process that had current performance cross-cutting aspects in problem identification because the issues were not categorized commensurate with their safety significance.  Notwithstanding  
were not timely.  The team identified two findings of very low significance related to the AR  
process that had current performance cross-cutting aspects in problem identification because  
the issues were not categorized commensurate with their safety significance.  Notwithstanding  
these two findings, the team concluded that in general Susquehanna personnel screened and  
these two findings, the team concluded that in general Susquehanna personnel screened and  
prioritized CRs in a timely manner using established criteria.   
prioritized CRs in a timely manner using established criteria.   
   
   
The team also concluded that Susquehanna personnel properly evaluated the issues commensurate with their safety significance; and generally implemented corrective actions in a timely manner, commensurate with the safety significance.  The team noted that Susquehanna  
The team also concluded that Susquehanna personnel properly evaluated the issues  
commensurate with their safety significance; and generally implemented corrective actions in a  
timely manner, commensurate with the safety significance.  The team noted that Susquehanna  
reviewed and applied industry operating experience lessons learned.  Audits and self-
reviewed and applied industry operating experience lessons learned.  Audits and self-
assessments added value to the corrective action process.  On the basis of interviews  
assessments added value to the corrective action process.  On the basis of interviews  
conducted during the inspection, workers at the site expressed freedom to enter safety concerns into the CAP.  
conducted during the inspection, workers at the site expressed freedom to enter safety  
 
concerns into the CAP.  
  Enclosure
   
3a. NRC Identified and Self-Revealing Findings
  Cornerstone: Mitigating Systems
  Green:  The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because, in the 1990s, Susquehanna failed to
 
adequately evaluate a deviation from the Boiling Water Reactor Owner's Group
Emergency Procedure Guidelines / Severe
Accident Guidelines (BWROG EPG/SAG), which resulted in one of the emergency operating procedures (EOPs) being inadequate.  Specifically, Caution #1 in the BWROG EPG/SAG warned the operators that reactor


Enclosure
3
a. NRC Identified and Self-Revealing Findings
Cornerstone:  Mitigating Systems
C
Green:  The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,
Instructions, Procedures, and Drawings, because, in the 1990s, Susquehanna failed to
adequately evaluate a deviation from the Boiling Water Reactor Owners Group
Emergency Procedure Guidelines / Severe Accident Guidelines (BWROG EPG/SAG),
which resulted in one of the emergency operating procedures (EOPs) being inadequate.
Specifically, Caution #1 in the BWROG EPG/SAG warned the operators that reactor
pressure vessel (RPV) level instrumentation may be unreliable if the drywell  
pressure vessel (RPV) level instrumentation may be unreliable if the drywell  
temperatures exceeded RPV saturation temperature.  The purpose of the Caution was  
temperatures exceeded RPV saturation temperature.  The purpose of the Caution was  
to give the operators a chance to evaluate the validity of the RPV level instrumentation  
to give the operators a chance to evaluate the validity of the RPV level instrumentation  
to avoid premature entry into the RPV flooding contingency procedure.  Susquehanna did not adequately evaluate the deviation, and the Susquehanna EOPs did not use a Caution statement; but instead, changed the caution to a procedural step, which directed  
to avoid premature entry into the RPV flooding contingency procedure.  Susquehanna  
did not adequately evaluate the deviation, and the Susquehanna EOPs did not use a  
Caution statement; but instead, changed the caution to a procedural step, which directed  
the operators to transition directly to the RPV flooding procedure.  
the operators to transition directly to the RPV flooding procedure.  
  The performance deficiency is more than minor because it is associated with the Procedure Quality attribute of the Mitigating Systems cornerstone and affects the objective to ensure the availability, reliability, and capability of systems that respond to  
   
The performance deficiency is more than minor because it is associated with the  
Procedure Quality attribute of the Mitigating Systems cornerstone and affects the  
objective to ensure the availability, reliability, and capability of systems that respond to  
initiating events to prevent undesirable consequences.  Specifically, the EOP could have  
initiating events to prevent undesirable consequences.  Specifically, the EOP could have  
directed entry into the RPV flooding procedure unnecessarily which would have  
directed entry into the RPV flooding procedure unnecessarily which would have  
restricted the use of suppression pool cooling and required other actions that would have  
restricted the use of suppression pool cooling and required other actions that would have  
complicated the operators' response to the event.  The finding was determined to be of very low safety significance because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to  
complicated the operators response to the event.  The finding was determined to be of  
very low safety significance because it was not a design deficiency, did not result in an  
actual loss of safety function, and did not screen as potentially risk significant due to  
external initiating events.  (Section 4OA2.a.3 (a))  
external initiating events.  (Section 4OA2.a.3 (a))  
 
  Green:  The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to identify that an inconsistency between the procedures and the design basis for suppression pool (SP) cooling was a condition  
C
Green:  The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion  
XVI, Corrective Action, for the failure to identify that an inconsistency between the  
procedures and the design basis for suppression pool (SP) cooling was a condition  
adverse to quality (CAQ), which resulted in corrective actions not being taken in a timely  
adverse to quality (CAQ), which resulted in corrective actions not being taken in a timely  
manner.  Specifically, in January 2006, a Condition Report (CR) identified an  
manner.  Specifically, in January 2006, a Condition Report (CR) identified an  
inconsistency between an assumption in the Final Safety Analysis Report (FSAR) for the  
inconsistency between an assumption in the Final Safety Analysis Report (FSAR) for the  
design basis accident and the emergency operating procedures (EOPs) regarding the timing for the implementation of SP cooling.  At the time of the inspection, the inconsistency had not been resolved because Susquehanna did not recognize that it  
design basis accident and the emergency operating procedures (EOPs) regarding the  
timing for the implementation of SP cooling.  At the time of the inspection, the  
inconsistency had not been resolved because Susquehanna did not recognize that it  
impacted current plant operations.  This performance deficiency has a cross-cutting  
impacted current plant operations.  This performance deficiency has a cross-cutting  
aspect in the area of Problem Identification and Resolution, Corrective Action Program,  
aspect in the area of Problem Identification and Resolution, Corrective Action Program,  
because Susquehanna did not identify that the inconsistency documented in the CR should have been categorized as a CAQ, commensurate with its safety significance.   
because Susquehanna did not identify that the inconsistency documented in the CR  
should have been categorized as a CAQ, commensurate with its safety significance.   
[P.1(a)]  
[P.1(a)]  
   
   
The performance deficiency is more than minor because it is associated with the Design  
The performance deficiency is more than minor because it is associated with the Design  
Control attribute of Mitigating Systems and affects the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to   
Control attribute of Mitigating Systems and affects the cornerstone objective to ensure  
  Enclosure  
the availability, reliability, and capability of systems that respond to initiating events to  
  4prevent undesirable consequences.  Specifical
 
ly, the EOPs provided direction that, under some accident conditions, would affect the availability and/or capability of the SP  
cooling system to perform its safety function.  The finding screened out as having very low safety significance because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to external  
   
Enclosure  
   
4
prevent undesirable consequences.  Specifically, the EOPs provided direction that,  
under some accident conditions, would affect the availability and/or capability of the SP  
cooling system to perform its safety function.  The finding screened out as having very  
low safety significance because it was not a design deficiency, did not result in an actual  
loss of safety function, and did not screen as potentially risk significant due to external  
initiating events.  (Section 4OA2.a.3 (b))  
initiating events.  (Section 4OA2.a.3 (b))  
   
   
Green:  The NRC identified a Non-Cited Violation of 10 CFR 55.46(c)(1), "Plant Referenced Simulators," because the Susquehanna simulator did not accurately model reactor pressure vessel (RPV) level instrumentation following a design basis accident  
C
Green:  The NRC identified a Non-Cited Violation of 10 CFR 55.46(c)(1), Plant  
Referenced Simulators, because the Susquehanna simulator did not accurately model  
reactor pressure vessel (RPV) level instrumentation following a design basis accident  
loss of coolant accident (DBA LOCA).  Specifically, an analysis performed in 1994 to  
loss of coolant accident (DBA LOCA).  Specifically, an analysis performed in 1994 to  
determine if the observed simulator response during a large break LOCA was consistent  
determine if the observed simulator response during a large break LOCA was consistent  
with the expected plant response, was based on an overly conservative assumption that  
with the expected plant response, was based on an overly conservative assumption that  
the drywell would experience superheated conditions, which would cause RPV water level instrumentation reference leg flashing and a subsequent loss of all RPV level indication.  The expected plant response, as stated in the analysis, was incorrect; in that  
the drywell would experience superheated conditions, which would cause RPV water  
level instrumentation reference leg flashing and a subsequent loss of all RPV level  
indication.  The expected plant response, as stated in the analysis, was incorrect; in that  
a LOCA would not always cause a loss of all RPV level instruments.  As a result, the  
a LOCA would not always cause a loss of all RPV level instruments.  As a result, the  
simulator modeling was incorrect.  
simulator modeling was incorrect.  
 
The performance deficiency is more than minor because it is associated with the Human Performance attribute of Mitigating Systems and affects the cornerstone objective to  
The performance deficiency is more than minor because it is associated with the Human  
Performance attribute of Mitigating Systems and affects the cornerstone objective to  
ensure the availability, reliability, and capability of systems that respond to initiating  
ensure the availability, reliability, and capability of systems that respond to initiating  
events to prevent undesirable consequences.  Specifically, the modeling of the  
events to prevent undesirable consequences.  Specifically, the modeling of the  
Susquehanna simulator introduced negative operator training that could affect the ability  
Susquehanna simulator introduced negative operator training that could affect the ability  
of the operators (a mitigating system) to take the appropriate actions during an actual event.  The finding was determined to be of very low safety significance because it is not related to operator performance during requalification, it is related to simulator fidelity,  
of the operators (a mitigating system) to take the appropriate actions during an actual  
event.  The finding was determined to be of very low safety significance because it is not  
related to operator performance during requalification, it is related to simulator fidelity,  
and it could have a negative impact on operator actions.    (Section 4OA2.a.3 (c))  
and it could have a negative impact on operator actions.    (Section 4OA2.a.3 (c))  
 
  Green:  The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to identify that a setpoint error in the operating procedures for safety-related systems was a condition adverse to quality (CAQ), resulting in the procedures not being corrected in a timely manner.  The setpoint for the  
C
Green:  The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion  
XVI, Corrective Action, for the failure to identify that a setpoint error in the operating  
procedures for safety-related systems was a condition adverse to quality (CAQ),  
resulting in the procedures not being corrected in a timely manner.  The setpoint for the  
low pressure injection permissive interlock in the RHR and CS systems had been  
low pressure injection permissive interlock in the RHR and CS systems had been  
changed in 1999 as part of a modification.  However, the setpoint was not changed in  
changed in 1999 as part of a modification.  However, the setpoint was not changed in  
the system operating procedures and operator aids.  When this issue was identified by Susquehanna staff in 2006, the setpoint error in the procedure was not screened as a CAQ, which resulted in the procedures not being revised for 17 months after the issue  
the system operating procedures and operator aids.  When this issue was identified by  
Susquehanna staff in 2006, the setpoint error in the procedure was not screened as a  
CAQ, which resulted in the procedures not being revised for 17 months after the issue  
was identified in an Action Report.  This performance deficiency has a cross-cutting  
was identified in an Action Report.  This performance deficiency has a cross-cutting  
aspect in the area of Problem Identification and Resolution, Corrective Action Program,  
aspect in the area of Problem Identification and Resolution, Corrective Action Program,  
because Susquehanna did not identify that a setpoint error in operating procedures for safety-related systems was a CAQ, commensurate with its safety significance.  [P.1(a)]  
because Susquehanna did not identify that a setpoint error in operating procedures for  
safety-related systems was a CAQ, commensurate with its safety significance.  [P.1(a)]  
   
   
The performance deficiency is more than minor because it is associated with the  
The performance deficiency is more than minor because it is associated with the  
Procedure Quality attribute of Mitigating Systems and affects the cornerstone objective  
Procedure Quality attribute of Mitigating Systems and affects the cornerstone objective  
to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  Specifically, the incorrect setpoint   
to ensure the availability, reliability, and capability of systems that respond to initiating  
  Enclosure  
events to prevent undesirable consequences.  Specifically, the incorrect setpoint  
  5reference in the procedure impacted the reliability of operator response to the event in that it could delay operator actions or result in misoperation of equipment.  The finding  
 
screened out as having very low safety significance because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to external initiating events.  (Section 4OA2.a.3 (e))  
  b. Licensee-Identified Violations
  None.   
   
  Enclosure  
Enclosure  
  6REPORT DETAILS
   
 
5
4. OTHER ACTIVITIES (OA)
reference in the procedure impacted the reliability of operator response to the event in  
  4OA2 Problem Identification and Resolution (PI&R) (Biennial - IP 71152B)
that it could delay operator actions or result in misoperation of equipment.  The finding  
 
screened out as having very low safety significance because it was not a design  
  a. Assessment of the Corrective Action Program
deficiency, did not result in an actual loss of safety function, and did not screen as  
    1. Inspection Scope
potentially risk significant due to external initiating events.  (Section 4OA2.a.3 (e))  
  The inspection team reviewed the procedures describing the corrective action program  
   
b. Licensee-Identified Violations  
None.  
 
   
Enclosure  
   
6
REPORT DETAILS  
4.  
OTHER ACTIVITIES (OA)  
4OA2 Problem Identification and Resolution (PI&R) (Biennial - IP 71152B)  
  a.  
Assessment of the Corrective Action Program  
  1.  
Inspection Scope  
The inspection team reviewed the procedures describing the corrective action program  
(CAP) at the Susquehanna Steam Electric Station.  Susquehanna used a single-point  
(CAP) at the Susquehanna Steam Electric Station.  Susquehanna used a single-point  
 
entry system and identified problems by the initiation of an Action Request (AR).  The  
entry system and identified problems by the initiation of an Action Request (AR).  The AR would then be sub-classified depending on the information provided; for example, as WO for a maintenance Work Order, as CPG for assignment to the Central Procedure Group, or as CR for a Condition Report.  ARs were sub-classified as CRs for conditions  
AR would then be sub-classified depending on the information provided; for example, as  
WO for a maintenance Work Order, as CPG for assignment to the Central Procedure  
Group, or as CR for a Condition Report.  ARs were sub-classified as CRs for conditions  
adverse to quality (CAQ), such as plant equipment deficiencies, industrial or radiological  
adverse to quality (CAQ), such as plant equipment deficiencies, industrial or radiological  
safety concerns, or other significant issues.  The CRs were subsequently screened for operability and reportability, categorized by significance (1 to 3), assigned a level of evaluation, and issued for resolution.  
safety concerns, or other significant issues.  The CRs were subsequently screened for  
  The team reviewed CRs selected across the seven cornerstones of safety in the NRC
operability and reportability, categorized by significance (1 to 3), assigned a level of  
=s Reactor Oversight Process (ROP) to determine if problems were being properly  
evaluation, and issued for resolution.  
   
The team reviewed CRs selected across the seven cornerstones of safety in the NRC=s  
Reactor Oversight Process (ROP) to determine if problems were being properly  
identified, characterized, and entered into the CAP for evaluation and resolution.  The  
identified, characterized, and entered into the CAP for evaluation and resolution.  The  
team selected items from the maintenance, operations, engineering, emergency  
team selected items from the maintenance, operations, engineering, emergency  
preparedness, physical security, radiation safety, training, and oversight programs to  
preparedness, physical security, radiation safety, training, and oversight programs to  
ensure that Susquehanna was appropriately considering problems identified in each  
ensure that Susquehanna was appropriately considering problems identified in each  
functional area.  The team used this information to select a risk-informed sample of CRs that had been issued since the last NRC PI&R inspection, which was conducted in  
functional area.  The team used this information to select a risk-informed sample of CRs  
that had been issued since the last NRC PI&R inspection, which was conducted in  
February 2006.  
February 2006.  
  The team selected ARs from other sub-classifications, to determine if Susquehanna had  
   
appropriately classified these items as not needing to be a CR.  The team also reviewed operator log entries, control room deficiency lists, operator work-around lists, operability determinations, engineering system health reports, completed surveillance tests, and  
The team selected ARs from other sub-classifications, to determine if Susquehanna had  
appropriately classified these items as not needing to be a CR.  The team also reviewed  
operator log entries, control room deficiency lists, operator work-around lists, operability  
determinations, engineering system health reports, completed surveillance tests, and  
current temporary configuration change packages.  In addition, the team interviewed  
current temporary configuration change packages.  In addition, the team interviewed  
plant staff and management to determine their understanding of and involvement with  
plant staff and management to determine their understanding of and involvement with  
 
the CAP at Susquehanna.  The CRs, and other documents reviewed, and the key  
the CAP at Susquehanna.  The CRs
personnel contacted, are listed in the Attachment to this report.  
, and other documents reviewed, and the key personnel contacted, are listed in the Attachment to this report.  
   
  The team considered risk insights from the NRC
The team considered risk insights from the NRC=s and Susquehanna=s risk analyses to  
=s and Susquehanna
focus the sample selection and plant tours on risk-significant components.  The team  
=s risk analyses to focus the sample selection and plant tours on risk-significant components.  The team determined that the five highest risk-significant systems at Susquehanna were emergency service water, emergency diesel generators, residual heat removal service  
determined that the five highest risk-significant systems at Susquehanna were  
emergency service water, emergency diesel generators, residual heat removal service  
water, station black-out diesel generator, and reactor core isolation cooling.  For the  
water, station black-out diesel generator, and reactor core isolation cooling.  For the  
risk-significant systems, the team reviewed a sample of the applicable system health
risk-significant systems, the team reviewed a sample of the applicable system health  
  Enclosure
7reports, work requests and engineering documents, plant log entries, and results from surveillance tests and maintenance tasks.


  The team reviewed CRs to assess whether Susquehanna adequately evaluated and prioritized the identified problems.  The CRs reviewed encompassed the full range of  
   
Susquehanna
=s causal evaluations, including root cause analyses (RCA - to determine the cause and prevent recurrence), apparent cause evaluations (ACE - to obtain a basic  
Enclosure
7
reports, work requests and engineering documents, plant log entries, and results from
surveillance tests and maintenance tasks.
The team reviewed CRs to assess whether Susquehanna adequately evaluated and  
prioritized the identified problems.  The CRs reviewed encompassed the full range of  
Susquehanna=s causal evaluations, including root cause analyses (RCA - to determine  
the cause and prevent recurrence), apparent cause evaluations (ACE - to obtain a basic  
understanding of the cause), and evaluations (to determine if a problem exists).  The  
understanding of the cause), and evaluations (to determine if a problem exists).  The  
review included the appropriateness of the assigned significance, the scope and depth  
review included the appropriateness of the assigned significance, the scope and depth  
of the causal analysis, and the timeliness of the resolutions.  For significant conditions  
of the causal analysis, and the timeliness of the resolutions.  For significant conditions  
adverse to quality, the team reviewed the effectiveness of the corrective actions to  
adverse to quality, the team reviewed the effectiveness of the corrective actions to  
prevent recurrence.  The team observed meetings of the CR Screening Team - in which Susquehanna personnel reviewed new CRs for prioritization, and evaluated preliminary corrective action assignments, analyses, and plans.  The team also attended meetings of the Corrective Action Review Board (CARB) - where senior managers reviewed selected evaluations, effectiveness reviews, and extension requests.   
prevent recurrence.  The team observed meetings of the CR Screening Team - in which  
 
Susquehanna personnel reviewed new CRs for prioritization, and evaluated preliminary  
The team reviewed equipment operability determinations, reportability assessments, and extent-of-condition reviews for selected problems.  The team assessed the backlog of  
corrective action assignments, analyses, and plans.  The team also attended meetings  
of the Corrective Action Review Board (CARB) - where senior managers reviewed  
selected evaluations, effectiveness reviews, and extension requests.   
The team reviewed equipment operability determinations, reportability assessments, and  
extent-of-condition reviews for selected problems.  The team assessed the backlog of  
corrective actions in the maintenance, engineering, and operations departments, to  
corrective actions in the maintenance, engineering, and operations departments, to  
determine, individually and collectively, if there was an increased risk due to delays in  
determine, individually and collectively, if there was an increased risk due to delays in  
implementation of corrective actions.  The team further reviewed equipment performance results and assessments documented in completed surveillance procedures, operator log entries, and trend data to determine whether the evaluations  
implementation of corrective actions.  The team further reviewed equipment  
performance results and assessments documented in completed surveillance  
procedures, operator log entries, and trend data to determine whether the evaluations  
were technically adequate to identify degrading or non-conforming equipment.  
were technically adequate to identify degrading or non-conforming equipment.  
  The team reviewed the corrective actions associated with selected CRs to determine if  
   
the actions addressed the identified causes of the problems.  The team reviewed CRs for significant repetitive problems to determine if previous corrective actions were  
The team reviewed the corrective actions associated with selected CRs to determine if  
effective.  The team also reviewed Susquehanna
the actions addressed the identified causes of the problems.  The team reviewed CRs  
=s timeliness in implementing corrective actions.  The team reviewed the CRs associated with selected non-cited violations (NCVs) and findings to determine if Susquehanna properly evaluated and resolved these  
for significant repetitive problems to determine if previous corrective actions were  
effective.  The team also reviewed Susquehanna=s timeliness in implementing corrective  
actions.  The team reviewed the CRs associated with selected non-cited violations  
(NCVs) and findings to determine if Susquehanna properly evaluated and resolved these  
issues.  
issues.  
  2. Assessment
    (a) Identification of Issues
  2.  
  In general, the team considered the identification of equipment deficiencies at  
Assessment  
  (a)  
Identification of Issues  
In general, the team considered the identification of equipment deficiencies at  
Susquehanna to be adequate.  There was a low threshold for the identification of  
Susquehanna to be adequate.  There was a low threshold for the identification of  
individual issues, 23,000 ARs were written per year, and about 4,000 of those were  
individual issues, 23,000 ARs were written per year, and about 4,000 of those were  
sub-classified as CRs.  The housekeeping and cleanliness of the plant was generally good; the general cleanliness of the plant enhanced the ability of personnel to more easily identify equipment deficiencies and monitor equipment for worsening conditions.  
sub-classified as CRs.  The housekeeping and cleanliness of the plant was generally  
good; the general cleanliness of the plant enhanced the ability of personnel to more  
easily identify equipment deficiencies and monitor equipment for worsening conditions.  
Notwithstanding, during a tour of the facility, the inspectors observed that high density
concrete shield blocks were stacked on pallets in the vicinity of the Unit 1 recirculation


   
   
Notwithstanding, during a tour of the facility, the inspectors observed that high density
concrete shield blocks were stacked on pallets in the vicinity of the Unit 1 recirculation  
   
  Enclosure  
Enclosure  
  8motor generator sets.  The blocks were pre-staged for work during the upcoming refueling outage, and were in a heavily trafficked area of the turbine building.  There was  
   
a painted warning on the floor, near the pallets, that the floor loading should not exceed 400 pounds per square foot (psf).  When the inspectors asked whether the weight of the blocks was within the rated floor load limit, it was determined that this condition had not  
8
motor generator sets.  The blocks were pre-staged for work during the upcoming  
refueling outage, and were in a heavily trafficked area of the turbine building.  There was  
a painted warning on the floor, near the pallets, that the floor loading should not exceed  
400 pounds per square foot (psf).  When the inspectors asked whether the weight of the  
blocks was within the rated floor load limit, it was determined that this condition had not  
been identified and documented as acceptable.  Initially, Susquehanna personnel  
been identified and documented as acceptable.  Initially, Susquehanna personnel  
concluded that the blocks exceeded the posted  
concluded that the blocks exceeded the posted limit and moved the pallets to reduce the  
limit and moved the pallets to reduce the floor loading.  Subsequently, Susquehanna weighed the pallets and blocks and determined that they did not exceed the allowable floor loading.  Based on this evaluation the inspectors concluded the missed identification of this issue was minor.   
floor loading.  Subsequently, Susquehanna weighed the pallets and blocks and  
determined that they did not exceed the allowable floor loading.  Based on this  
evaluation the inspectors concluded the missed identification of this issue was minor.   
The issue was documented in CR 954950.  
The issue was documented in CR 954950.  
   
   
The team also identified that several ARs were not classified as CRs, commensurate  
The team also identified that several ARs were not classified as CRs, commensurate  
with the safety significance, as required by their procedure (NDAP-QA-0702, "Action Request and Condition Report Process").  The result was that the issues did not go to  
with the safety significance, as required by their procedure (NDAP-QA-0702, Action  
the Screening Team, did not receive the necessary management attention, and were not corrected in a timely manner (CR 957319).  In addition, ARs are not normally trended to  
Request and Condition Report Process).  The result was that the issues did not go to  
the Screening Team, did not receive the necessary management attention, and were not  
corrected in a timely manner (CR 957319).  In addition, ARs are not normally trended to  
allow the identification of an adverse change in performance.  With the exception of the  
allow the identification of an adverse change in performance.  With the exception of the  
first example, the below are considered procedure violations of minor significance due to no impact on the related equipment.  As such, these issues are not subject to enforcement action, in accordance with the NRC
first example, the below are considered procedure violations of minor significance due to  
=s Enforcement Policy.  
no impact on the related equipment.  As such, these issues are not subject to  
  Examples include:  
enforcement action, in accordance with the NRC=s Enforcement Policy.  
   
Examples include:  
   
   
AR/CPG/OPS 751412, initiated February 2, 2006, identified that the Low Pressure Injection Permissive setpoint was not changed in the residual heat removal (RHR)  
C
AR/CPG/OPS 751412, initiated February 2, 2006, identified that the Low Pressure  
Injection Permissive setpoint was not changed in the residual heat removal (RHR)  
and core spray (CS) operating procedures.  The setpoint was changed in 1999, as  
and core spray (CS) operating procedures.  The setpoint was changed in 1999, as  
part of a modification; the procedures were not changed until July 2007.  (See Section 4OA2.a.3(d) for additional details.)  
part of a modification; the procedures were not changed until July 2007.  (See  
Section 4OA2.a.3(d) for additional details.)  
   
   
AR/OPS/CSHIFT 777335, initiated July 25 2006, identified that an operator started the suppression pool (SP) filter pump contrary to the procedure.  The AR was closed  
C
AR/OPS/CSHIFT 777335, initiated July 25 2006, identified that an operator started  
the suppression pool (SP) filter pump contrary to the procedure.  The AR was closed  
with no documented corrective actions taken.   
with no documented corrective actions taken.   
  The safety significance is that the operator did not operate the safety-related system  
   
in accordance with the licensee's written procedures and the Technical  
The safety significance is that the operator did not operate the safety-related system  
in accordance with the licensees written procedures and the Technical  
Specifications (TS).  The documentation of corrective actions should have included a  
Specifications (TS).  The documentation of corrective actions should have included a  
determination of the affects of starting of the pump, and counseling of the operator  
determination of the affects of starting of the pump, and counseling of the operator  
on the requirement to follow procedures.
C
AR/CPG 810513, initiated September 16, 2006, identified that the wrong valve
numbers were listed for the emergency service water (ESW) system valves for the
E EDG.  As of the inspection, the procedure had not been changed. 
The safety significance is that operators may not have been able to use the
licensees written procedure to align the ESW system in support of the operation of
the swing E EDG in a timely manner.


on the requirement to follow procedures.
   
  AR/CPG 810513, initiated September 16, 2006, identified that the wrong valve numbers were listed for the emergency service water (ESW) system valves for the
   
"E" EDG. As of the inspection, the procedure had not been changed. 
   
  The safety significance is that operators may not have been able to use the licensee's written procedure to align the ESW system in support of the operation of
Enclosure  
the swing "E" EDG in a timely manner.  
   
  Enclosure  
9
  9  AR/CPG/I&C 938054, initiated December 10, 2007, identified that a functional testing and calibration procedure for the RHR service water radiation monitor could not be performed, as written.  As of the inspection, corrective actions had not been taken.  
   
C
AR/CPG/I&C 938054, initiated December 10, 2007, identified that a functional testing  
and calibration procedure for the RHR service water radiation monitor could not be  
performed, as written.  As of the inspection, corrective actions had not been taken.  
   
   
an inconsistency between the procedures and the design basis for SP cooling was a  
an inconsistency between the procedures and the design basis for SP cooling was a  
CAQ, which resulted in corrective actions not being taken for two years to the time of the  
CAQ, which resulted in corrective actions not being taken for two years to the time of the  
inspection.  Although the inconsistency was identified in 2006, Susquehanna personnel did not recognize that the issue impacted current plant operations; as a result, the issue was not scheduled for resolution in a timely manner.  The team noted that, although  
inspection.  Although the inconsistency was identified in 2006, Susquehanna personnel  
Susquehanna had classified the issue as a CR, it was considered to be "NAQ" - not a  
did not recognize that the issue impacted current plant operations; as a result, the issue  
was not scheduled for resolution in a timely manner.  The team noted that, although  
Susquehanna had classified the issue as a CR, it was considered to be NAQ - not a  
CAQ - and was not scheduled for evaluation until the EPU had been approved.  Refer to  
CAQ - and was not scheduled for evaluation until the EPU had been approved.  Refer to  
Section 4OA2.a.3(b) for a detailed discussion of the finding.  
Section 4OA2.a.3(b) for a detailed discussion of the finding.  
    (b) Prioritization and Evaluation of Issues
  The team determined that Susquehanna's performance in this area was adequate.   
  (b)  
Prioritization and Evaluation of Issues  
The team determined that Susquehannas performance in this area was adequate.   
Notwithstanding the above discussion of some ARs not being classified as CRs, the  
Notwithstanding the above discussion of some ARs not being classified as CRs, the  
station appropriately reviewed those CRs that went to the Screening team and properly classified them for significance.  The discussions about specific topics at the Screening meetings were detailed, and there were no classifications or immediate operability  
station appropriately reviewed those CRs that went to the Screening team and properly  
classified them for significance.  The discussions about specific topics at the Screening  
meetings were detailed, and there were no classifications or immediate operability  
determinations with which the team disagreed.  The team considered the contributions of  
determinations with which the team disagreed.  The team considered the contributions of  
the CARB to add value to the CAP process.  One CARB review was noted to be  
the CARB to add value to the CAP process.  One CARB review was noted to be  
particularly insightful with respect to the quality of the causal analysis for CR 773046.   
particularly insightful with respect to the quality of the causal analysis for CR 773046.   
The CR identified problems with the closing of CRs by the nuclear training department without completing all the required actions.  The team did not identify any items in the operations, engineering, or maintenance backlogs that were risk significant, individually  
The CR identified problems with the closing of CRs by the nuclear training department  
without completing all the required actions.  The team did not identify any items in the  
operations, engineering, or maintenance backlogs that were risk significant, individually  
or collectively.  In addition, the quality of the causal analyses reviewed was generally of  
or collectively.  In addition, the quality of the causal analyses reviewed was generally of  
adequate technical detail and scope to identify causal factors and develop effective  
adequate technical detail and scope to identify causal factors and develop effective  
corrective actions.  The team noted that the RCA for the NCV from the last PI&R inspection related to scaffolding was effective in that there had not been significant recurrences of inadequate scaffold installations since the evaluation was completed.  
corrective actions.  The team noted that the RCA for the NCV from the last PI&R  
 
inspection related to scaffolding was effective in that there had not been significant  
recurrences of inadequate scaffold installations since the evaluation was completed.  
   
   
With regard to operability evaluations, the team observed that, an operability  
With regard to operability evaluations, the team observed that, an operability  
determination for the PAM level instruments, conducted in response to an inconsistency  
determination for the PAM level instruments, conducted in response to an inconsistency  
between the FSAR and EOPs, determined that the level instruments would be operable.  (The inconsistency between the FSAR and the EOPs is described in detail in section 4OA2.a.3(b).)  During follow-up discussions, the inspectors were told by operations and  
between the FSAR and EOPs, determined that the level instruments would be operable.  
  (The inconsistency between the FSAR and the EOPs is described in detail in section  
4OA2.a.3(b).)  During follow-up discussions, the inspectors were told by operations and  
engineering personnel that all of the PAM instrumentation together functioned to provide  
engineering personnel that all of the PAM instrumentation together functioned to provide  
the needed indications to the operators, and that the RPV level indications were not  
the needed indications to the operators, and that the RPV level indications were not  
needed after the initial entry into the EOPs.  This was not consistent with the requirements for the operability of each individual function of the PAM, as detailed in TS 3.3.3.1.  Although subsequent discussions with the Susquehanna staff determined that  
needed after the initial entry into the EOPs.  This was not consistent with the  
requirements for the operability of each individual function of the PAM, as detailed in TS  
3.3.3.1.  Although subsequent discussions with the Susquehanna staff determined that  
the most (if not all) of the PAM RPV level instruments would indicate post-LOCA, the  
the most (if not all) of the PAM RPV level instruments would indicate post-LOCA, the  
initial operability determination and statements during the inspection did not consider  
initial operability determination and statements during the inspection did not consider  
that the PAM level instruments are required to be operable post-accident regardless of whether EOPs have been entered.  This issue was related to the performance
that the PAM level instruments are required to be operable post-accident regardless of  
  Enclosure
whether EOPs have been entered.  This issue was related to the performance  
10deficiencies discussed in findings 4OA2.a.3(a), (b) and (c), and is not identified as an additional finding.  The issue was entered into the CAP as AR/CR964836.


    (c) Effectiveness of Corrective Actions
  No findings of significance were identified in the area of effectiveness of corrective  
Enclosure
10
deficiencies discussed in findings 4OA2.a.3(a), (b) and (c), and is not identified as an
additional finding.  The issue was entered into the CAP as AR/CR964836.
  (c)
Effectiveness of Corrective Actions  
No findings of significance were identified in the area of effectiveness of corrective  
actions.  The team determined that the effectiveness of corrective actions at  
actions.  The team determined that the effectiveness of corrective actions at  
Susquehanna was generally good.  The control of scaffolds was a significant problem during the last PI&R inspection; the team noted that oversight of scaffolds has improved, but station personnel continue to identify examples where the scaffold does not appear  
Susquehanna was generally good.  The control of scaffolds was a significant problem  
during the last PI&R inspection; the team noted that oversight of scaffolds has improved,  
but station personnel continue to identify examples where the scaffold does not appear  
to be built in accordance with the procedure.  In addition, the team identified  
to be built in accordance with the procedure.  In addition, the team identified  
weaknesses in the scaffold procedure, such as allowing the installer to approve  
weaknesses in the scaffold procedure, such as allowing the installer to approve  
deviations from the approved construction.  During the inspection, the procedure was  
deviations from the approved construction.  During the inspection, the procedure was  
revised, and plans were developed for engineering to review all current deviations.  
revised, and plans were developed for engineering to review all current deviations.  
  3. Findings
 
  3.  
   (a) Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an  
Findings  
Inadequate Procedure
  Introduction:  The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," because Susquehanna failed to adequately  
   (a)  
 
Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an  
evaluate a deviation from the Boiling Water Reactor Owner's Group Emergency  
Inadequate Procedure  
Procedure Guidelines / Severe Accident  
Guidelines (BWROG EPG/SAG), which resulted in one of the Emergency Operating Procedures (EOPs) being inadequate.  
Introduction:  The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion V,  
  Description:  On January 5, 2006, AR/CR 739371 was initiated to document an inconsistency between the EOPs and assumptions in the Final Safety Analysis Report  
Instructions, Procedures, and Drawings, because Susquehanna failed to adequately  
evaluate a deviation from the Boiling Water Reactor Owners Group Emergency  
Procedure Guidelines / Severe Accident Guidelines (BWROG EPG/SAG), which  
resulted in one of the Emergency Operating Procedures (EOPs) being inadequate.  
   
Description:  On January 5, 2006, AR/CR 739371 was initiated to document an  
inconsistency between the EOPs and assumptions in the Final Safety Analysis Report  
(FSAR) regarding the initiation of suppression pool cooling.  Specifically, it was identified  
(FSAR) regarding the initiation of suppression pool cooling.  Specifically, it was identified  
that the assumptions used in evaluating SP temperature response for the most limiting design basis accident (DBA) loss of coolant accident (LOCA) did not appear to be consistent with direction provided in the EOPs.  
that the assumptions used in evaluating SP temperature response for the most limiting  
 
design basis accident (DBA) loss of coolant accident (LOCA) did not appear to be  
consistent with direction provided in the EOPs.  
   
   
During this inspection, the team noted that the Susquehanna EOPs were not consistent  
During this inspection, the team noted that the Susquehanna EOPs were not consistent  
with the BWROG EPG/SAG.  Specifically, BWROG EPG/SAG, Revision 2, Caution #1, warned the operators that reactor pressure vessel (RPV) level instrumentation may be unreliable if the temperatures near the instrument sensing lines exceeded RPV saturation temperature.  The EPG Bases stated that the purpose of Caution #1 was to  
with the BWROG EPG/SAG.  Specifically, BWROG EPG/SAG, Revision 2, Caution #1,  
warned the operators that reactor pressure vessel (RPV) level instrumentation may be  
unreliable if the temperatures near the instrument sensing lines exceeded RPV  
saturation temperature.  The EPG Bases stated that the purpose of Caution #1 was to  
give the operators a chance to evaluate the validity of the RPV level instrumentation, in  
give the operators a chance to evaluate the validity of the RPV level instrumentation, in  
order to avoid premature entry into the RPV flooding contingency procedure before it  
order to avoid premature entry into the RPV flooding contingency procedure before it  
was appropriate to do so.  Susquehanna did not adequately evaluate the deviation from the generic guidance in the EPG/SAG with respect to the caution.  The Susquehanna EOPs did not use a Caution statement, which would have allowed the operators the  
was appropriate to do so.  Susquehanna did not adequately evaluate the deviation from  
the generic guidance in the EPG/SAG with respect to the caution.  The Susquehanna  
EOPs did not use a Caution statement, which would have allowed the operators the  
opportunity to evaluate the level instrumentation; but instead, changed the caution to a  
opportunity to evaluate the level instrumentation; but instead, changed the caution to a  
procedural step which directed the operators to transition directly to the RPV Flooding  
procedural step which directed the operators to transition directly to the RPV Flooding  
procedure.  Specifically, EO-100-103-1, "Primary Containment Cooling," step DWT-3,   
procedure.  Specifically, EO-100-103-1, Primary Containment Cooling, step DWT-3,  
  Enclosure  
 
  11directed the operators to transition to contingency procedure EO-000-114-1, "RPV  
Flooding," when drywell temperature exceeded RPV saturation temperature.  
  The evaluation for the deviation was not completed in accordance with the requirements of procedure NDAP-QA-0330, "Symptom Oriented EOP and EP-DS Program and  
   
Writer's Guide." The procedure required that all deviations be evaluated to determine if  
Enclosure  
the deviation was technically justifie
   
d and appropriate.  Susquehanna documented that the deviation was a minor "difference" from the generic guidelines in 50.59 Safety  
11
directed the operators to transition to contingency procedure EO-000-114-1, RPV  
Flooding, when drywell temperature exceeded RPV saturation temperature.  
   
The evaluation for the deviation was not completed in accordance with the requirements  
of procedure NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and  
Writers Guide.  The procedure required that all deviations be evaluated to determine if  
the deviation was technically justified and appropriate.  Susquehanna documented that  
the deviation was a minor difference from the generic guidelines in 50.59 Safety  
Evaluation NL-92-019 (October 29, 1998) and 50.59 Screen 5059-01-976 (July 3, 2002).  
Evaluation NL-92-019 (October 29, 1998) and 50.59 Screen 5059-01-976 (July 3, 2002).  
  The evaluation was based on an overly conservative assumption that all RPV level  
  The evaluation was based on an overly conservative assumption that all RPV level  
Line 395: Line 657:
potential adverse consequences associated with the deviation, including the potential  
potential adverse consequences associated with the deviation, including the potential  
impact on the SP cooling safety function.  Immediate corrective actions included the  
impact on the SP cooling safety function.  Immediate corrective actions included the  
initiation of an informational Night Order to the control room operators explaining the issue, and the cessation of all simulator scenarios that involve the use of EO-100-103-1 until the issue is resolved.  
initiation of an informational Night Order to the control room operators explaining the  
 
issue, and the cessation of all simulator scenarios that involve the use of EO-100-103-1  
until the issue is resolved.  
   
   
The performance deficiency is the failure to adequately evaluate a deviation from the  
The performance deficiency is the failure to adequately evaluate a deviation from the  
BWROG EPG/SAG, which resulted in one of the EOPs being inadequate for use by the operators in the event of a DBA LOCA.  Specifically, under some accident conditions, the EOPs would have unnecessarily directed entry into RPV flooding which would have limited the availability of SP cooling and complicated the operators' response to the  
BWROG EPG/SAG, which resulted in one of the EOPs being inadequate for use by the  
 
operators in the event of a DBA LOCA.  Specifically, under some accident conditions,  
the EOPs would have unnecessarily directed entry into RPV flooding which would have  
limited the availability of SP cooling and complicated the operators response to the  
event.  
event.  
   
   
Analyses:  This performance deficiency is more than minor because it is associated with the Procedure Quality (EOP) attribute of the Mitigating Systems cornerstone and affects the objective to ensure the availability, reliability, and capability of systems that respond  
Analyses:  This performance deficiency is more than minor because it is associated with  
the Procedure Quality (EOP) attribute of the Mitigating Systems cornerstone and affects  
the objective to ensure the availability, reliability, and capability of systems that respond  
to initiating events to prevent undesirable consequences.  Specifically, the EOP could  
to initiating events to prevent undesirable consequences.  Specifically, the EOP could  
have directed entry into the RPV flooding procedure unnecessarily which would have restricted the use of suppression pool cooling and required other actions that would have complicated the operators' response to the event.  The inspectors performed a review of the finding in accordance with NRC Inspection Manual Chapter (IMC) 0609,  
have directed entry into the RPV flooding procedure unnecessarily which would have  
"Significance Determination Process (SDP)," Attachment 4, "Phase 1 - Initial Screening  
restricted the use of suppression pool cooling and required other actions that would have  
and Characterization of Findings," and determined that the finding screened out as  
complicated the operators response to the event.  The inspectors performed a review of  
the finding in accordance with NRC Inspection Manual Chapter (IMC) 0609,  
Significance Determination Process (SDP), Attachment 4, Phase 1 - Initial Screening  
and Characterization of Findings, and determined that the finding screened out as  
having very low safety significance (Green), because it was not a design deficiency, did  
having very low safety significance (Green), because it was not a design deficiency, did  
not result in an actual loss of safety function, and did not screen as potentially risk significant due to external initiating events.  
not result in an actual loss of safety function, and did not screen as potentially risk  
  Enforcement:  10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," states, in part, that activities affecting quality shall be prescribed by  
significant due to external initiating events.  
documented procedures appropriate to the circumstances and that the activities shall be accomplished in accordance with the procedures.  Contrary to the above, Emergency Operating Procedure EO-100-103-1, "Primary Containment Cooling," was inadequate, in  
   
Enforcement:  10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and  
Drawings, states, in part, that activities affecting quality shall be prescribed by  
documented procedures appropriate to the circumstances and that the activities shall be  
accomplished in accordance with the procedures.  Contrary to the above, Emergency  
Operating Procedure EO-100-103-1, Primary Containment Cooling, was inadequate, in  
that it directed the operators to transition directly to the RPV Flooding procedure when  
that it directed the operators to transition directly to the RPV Flooding procedure when  
RPV level instruments may have been available, which resulted in limiting the availability of SP cooling.  However, because the finding was of very low safety significance (Green)   
RPV level instruments may have been available, which resulted in limiting the availability  
  Enclosure  
of SP cooling.  However, because the finding was of very low safety significance (Green)  
  12and has been entered into the CAP (AR/CR 962881), this violation is being treated as an NCV, consistent with section VI.A.1 of the NRC Enforcement Policy.  
 
  (NCV 05000387/2008006-01; 05000388/2008006-01 - Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an Inadequate EOP)
    (b) Failure to Identify and Correct Inconsistencies Between the FSAR and the EOPs
  Introduction:  The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to identify that an inconsistency between the  
   
Enclosure  
   
12
and has been entered into the CAP (AR/CR 962881), this violation is being treated as an  
NCV, consistent with section VI.A.1 of the NRC Enforcement Policy.  
   
(NCV 05000387/2008006-01; 05000388/2008006-01 - Failure to Adequately Evaluate  
a Deviation from BWROG EPG/SAG Resulted in an Inadequate EOP)  
  (b)  
Failure to Identify and Correct Inconsistencies Between the FSAR and the EOPs  
Introduction:  The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI,  
Corrective Action, for the failure to identify that an inconsistency between the  
emergency operating procedures and the design basis for SP cooling was a CAQ, which  
emergency operating procedures and the design basis for SP cooling was a CAQ, which  
resulted in corrective actions not being taken for two years to the time of the inspection.   
resulted in corrective actions not being taken for two years to the time of the inspection.   
Although the inconsistency was identified in 2006, Susquehanna personnel did not  
Although the inconsistency was identified in 2006, Susquehanna personnel did not  
recognize that the issue impacted current plant operations; as a result, the issue was not scheduled for resolution in a timely manner.  The assumption in the FSAR for the DBA LOCA stated that SP cooling would be implemented ten minutes after entry into the  
recognize that the issue impacted current plant operations; as a result, the issue was not  
scheduled for resolution in a timely manner.  The assumption in the FSAR for the DBA  
LOCA stated that SP cooling would be implemented ten minutes after entry into the  
EOPs. The EOPs would not have allowed initiation of SP cooling for an extended period  
EOPs. The EOPs would not have allowed initiation of SP cooling for an extended period  
of time.   
of time.   
 
Description:  On January 5, 2006, AR/CR 739371 was initiated to document an inconsistency between the EOPs and design basis assumptions for the SP cooling  
Description:  On January 5, 2006, AR/CR 739371 was initiated to document an  
response.  The problem was identified during Susquehanna's review in support of the  
inconsistency between the EOPs and design basis assumptions for the SP cooling  
response.  The problem was identified during Susquehannas review in support of the  
extended power uprate (EPU) project.  Specifically, Susquehanna Engineering identified  
extended power uprate (EPU) project.  Specifically, Susquehanna Engineering identified  
that the assumptions used in evaluating SP temperature response for the most limiting  
that the assumptions used in evaluating SP temperature response for the most limiting  
LOCA did not appear to be consistent with direction provided in the EOPs.  The team noted that, although Susquehanna personnel had classified the issue as a CR, they did not recognize that the issue impacted current plant operations.  Therefore, it was  
LOCA did not appear to be consistent with direction provided in the EOPs.  The team  
considered to be "NAQ" - not a condition adverse to quality - and was not scheduled for  
noted that, although Susquehanna personnel had classified the issue as a CR, they did  
not recognize that the issue impacted current plant operations.  Therefore, it was  
considered to be NAQ - not a condition adverse to quality - and was not scheduled for  
evaluation until the EPU had been approved.  
evaluation until the EPU had been approved.  
 
The Susquehanna FSAR, Section 6.2.1.1.3, stated that the maximum SP temperature would result from a reactor recirculation suction line break.  The drywell pressure and  
The Susquehanna FSAR, Section 6.2.1.1.3, stated that the maximum SP temperature  
would result from a reactor recirculation suction line break.  The drywell pressure and  
temperature response analyses assumed that RHR heat exchangers were activated  
temperature response analyses assumed that RHR heat exchangers were activated  
about ten minutes after entry into the EOPs to remove energy from the drywell by  
about ten minutes after entry into the EOPs to remove energy from the drywell by  
cooling the SP.  The CR identified that, in the event of a DBA LOCA, the EOPs would  
cooling the SP.  The CR identified that, in the event of a DBA LOCA, the EOPs would  
direct operators to implement the RPV flooding procedure (EO-000-114) to maintain  
direct operators to implement the RPV flooding procedure (EO-000-114) to maintain  
adequate core cooling, and this required that
adequate core cooling, and this required that all available RHR flow be used to flood the  
all available RHR flow be used to flood the RPV up to the steam lines.  The initiator's concern was that this would delay establishing  
RPV up to the steam lines.  The initiators concern was that this would delay establishing  
flow through a RHR heat exchanger for SP cooling, because of the unique design of the RHR system at Susquehanna, and therefore w
flow through a RHR heat exchanger for SP cooling, because of the unique design of the  
ould be inconsistent with the accident analyses assumptions.  In addition, the CR stated that it was assumed in the EOPs that all RPV water level indications would be unreliable and therefore unavailable for this scenario.  Susquehanna personnel informed the team that they had not evaluated the  
RHR system at Susquehanna, and therefore would be inconsistent with the accident  
analyses assumptions.  In addition, the CR stated that it was assumed in the EOPs that  
all RPV water level indications would be unreliable and therefore unavailable for this  
scenario.  Susquehanna personnel informed the team that they had not evaluated the  
issues documented in the CR, at the time it was initiated, because they had assumed  
issues documented in the CR, at the time it was initiated, because they had assumed  
that they were only associated with EPU and not current plant operation.  Immediate  
that they were only associated with EPU and not current plant operation.  Immediate  
corrective actions included the start of an evaluation during the inspection of the identified inconsistency for SP cooling, and additional guidance to the operators.
corrective actions included the start of an evaluation during the inspection of the  
  Enclosure
identified inconsistency for SP cooling, and additional guidance to the operators.  
13 The performance deficiency is the failure to properly categorize the inconsistency
 
between the FSAR and the EOPs as a CAQ, which resulted in the deficiency not being corrected in a timely manner commensurate with its safety significance. 
   
   
Analyses:  The performance deficiency is more than minor because it is associated with the Design Control attribute of the Mitigating Systems cornerstone and affects the  
objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences.  Specifically, in the event of a DBA LOCA, SP cooling would not be initiated within the time frame assumed in the  
Enclosure
13
The performance deficiency is the failure to properly categorize the inconsistency
between the FSAR and the EOPs as a CAQ, which resulted in the deficiency not being
corrected in a timely manner commensurate with its safety significance. 
Analyses:  The performance deficiency is more than minor because it is associated with  
the Design Control attribute of the Mitigating Systems cornerstone and affects the  
objective to ensure the availability, reliability, and capability of systems that respond to  
initiating events to prevent undesirable consequences.  Specifically, in the event of a  
DBA LOCA, SP cooling would not be initiated within the time frame assumed in the  
FSAR, which could affect the capability of the system to perform its safety function  
FSAR, which could affect the capability of the system to perform its safety function  
consistent with the design basis.  The inspectors performed a review of the finding in  
consistent with the design basis.  The inspectors performed a review of the finding in  
accordance with IMC 0609, and determined that the finding screened out as having very  
accordance with IMC 0609, and determined that the finding screened out as having very  
low safety significance (Green) because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to  
low safety significance (Green) because it was not a design deficiency, did not result in  
an actual loss of safety function, and did not screen as potentially risk significant due to  
external initiating events.  
external initiating events.  
   
   
This performance deficiency has a cross-cutting aspect in the area of Problem  
This performance deficiency has a cross-cutting aspect in the area of Problem  
Identification and Resolution (PI&R), Corrective Action Program (CAP), because Susquehanna did not identify that the inconsistency documented in the CR should have been categorized as a CAQ, commensurate with its safety significance.  [P.1(a)]  
Identification and Resolution (PI&R), Corrective Action Program (CAP), because  
  Enforcement:  10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," states, in part, that conditions adverse to quality shall be promptly identified and corrected.  Contrary to  
Susquehanna did not identify that the inconsistency documented in the CR should have  
the above, Susquehanna failed to identify that the nonconformance identified in AR/CR 739371, January 2006, was a CAQ; this resulted in the condition not being corrected for over two years.  However, because the finding was of very low safety significance  
been categorized as a CAQ, commensurate with its safety significance.  [P.1(a)]  
   
Enforcement:  10 CFR 50, Appendix B, Criterion XVI, Corrective Action, states, in part,  
that conditions adverse to quality shall be promptly identified and corrected.  Contrary to  
the above, Susquehanna failed to identify that the nonconformance identified in AR/CR  
739371, January 2006, was a CAQ; this resulted in the condition not being corrected for  
over two years.  However, because the finding was of very low safety significance  
(Green) and has been entered into the corrective action program (AR/CR 959670), this  
(Green) and has been entered into the corrective action program (AR/CR 959670), this  
violation is being treated as an NCV, consistent with section VI.A.1 of the NRC  
violation is being treated as an NCV, consistent with section VI.A.1 of the NRC  
 
Enforcement Policy.  
Enforcement Policy.   
   
(NCV 05000387/2008006-02; 05000388/2008006-02 - Failure to Identify and Correct  
(NCV 05000387/2008006-02; 05000388/2008006-02 - Failure to Identify and Correct  
Inconsistencies Between the FSAR and the EOPs)  
Inconsistencies Between the FSAR and the EOPs)  
 
    (c) Failure to Accurately Model the Simulator for RPV Water Level Instrumentation
  (c)  
  Introduction:  The NRC identified a Green NCV of 10 CFR 55.46(c)(1), "Plant Referenced Simulators," because the Susquehanna plant-referenced simulator did not  
Failure to Accurately Model the Simulator for RPV Water Level Instrumentation  
accurately model RPV level instrument response following a DBA LOCA.  Specifically, the RPV level instruments in the simulator were programmed to fail high after a LOCA,  
Introduction:  The NRC identified a Green NCV of 10 CFR 55.46(c)(1), Plant  
Referenced Simulators, because the Susquehanna plant-referenced simulator did not  
accurately model RPV level instrument response following a DBA LOCA.  Specifically,  
the RPV level instruments in the simulator were programmed to fail high after a LOCA,  
and the expected plant response is that the instruments should indicate properly.  
and the expected plant response is that the instruments should indicate properly.  
  Description:  As part of the team's follow-up on the issues in AR/CR 739371, the inspectors questioned the concern stated in the CR, that the operators would need to  
   
Description:  As part of the teams follow-up on the issues in AR/CR 739371, the  
inspectors questioned the concern stated in the CR, that the operators would need to  
enter the RPV flooding procedure during a DBA LOCA due to a loss of valid RPV level  
enter the RPV flooding procedure during a DBA LOCA due to a loss of valid RPV level  
instrumentation.  The inspectors reviewed the Susquehanna specific EOPs and supporting documents, and determined that the Susquehanna EOP Plant Specific   
instrumentation.  The inspectors reviewed the Susquehanna specific EOPs and  
  Enclosure  
supporting documents, and determined that the Susquehanna EOP Plant Specific  
  14Technical Guideline (PSTG) description of the expected response of the RPV level instrument response to LOCA events, was based on analysis, EC-SIMU-1001,  
 
"Evaluation of Simulator Level Instrument Response to Large LOCA," dated May 4, 1994.  The analysis was performed to determine if the observed simulator response during a large break LOCA (RPV level instrumentation off-scale high) was consistent  
   
Enclosure  
   
14
Technical Guideline (PSTG) description of the expected response of the RPV level  
instrument response to LOCA events, was based on analysis, EC-SIMU-1001,  
Evaluation of Simulator Level Instrument Response to Large LOCA, dated May 4,  
1994.  The analysis was performed to determine if the observed simulator response  
during a large break LOCA (RPV level instrumentation off-scale high) was consistent  
with the expected plant response.  The analysis assumed that the drywell would  
with the expected plant response.  The analysis assumed that the drywell would  
experience superheated conditions, which would cause RPV water level instrumentation  
experience superheated conditions, which would cause RPV water level instrumentation  
reference leg flashing and a subsequent loss of all RPV level indication.  The analysis concluded that the simulator response reasonably predicted the expected actual plant response during a large break LOCA event.  The expected plant response, as stated in  
reference leg flashing and a subsequent loss of all RPV level indication.  The analysis  
concluded that the simulator response reasonably predicted the expected actual plant  
response during a large break LOCA event.  The expected plant response, as stated in  
the analysis, was incorrect; in that a LOCA would not always cause a loss of all RPV  
the analysis, was incorrect; in that a LOCA would not always cause a loss of all RPV  
level instruments.  
level instruments.  
  On January 29, 2008, the inspectors observed two scenarios in the simulator to evaluate the response to a DBA LOCA, with all safe
   
ty systems available.  The inspectors observed that the RPV level instruments did indicate off-scale high shortly after the  
On January 29, 2008, the inspectors observed two scenarios in the simulator to evaluate  
the response to a DBA LOCA, with all safety systems available.  The inspectors  
observed that the RPV level instruments did indicate off-scale high shortly after the  
initiation of the event, consistent with the analysis.  The inspectors questioned the basis  
initiation of the event, consistent with the analysis.  The inspectors questioned the basis  
of the analysis; specifically, why Susquehanna believed that the level instruments would  
of the analysis; specifically, why Susquehanna believed that the level instruments would  
not be available after a DBA LOCA event.  Subsequently, Susquehanna determined that the RPV level instrument reference legs were not expected to routinely flash during a DBA LOCA, and that the analysis had been based on an overly conservative assumption  
not be available after a DBA LOCA event.  Subsequently, Susquehanna determined that  
the RPV level instrument reference legs were not expected to routinely flash during a  
DBA LOCA, and that the analysis had been based on an overly conservative assumption  
that the drywell would always reach superheated conditions post-LOCA.  Immediate  
that the drywell would always reach superheated conditions post-LOCA.  Immediate  
corrective actions included the initiation of an informational Night Order to the control  
corrective actions included the initiation of an informational Night Order to the control  
room operators explaining the issue, and the cessation of all simulator scenarios that  
room operators explaining the issue, and the cessation of all simulator scenarios that  
involve the use of EO-100-103-1 until the issue is resolved.  
involve the use of EO-100-103-1 until the issue is resolved.  
  The performance deficiency is that Susquehanna did not ensure that the plant  
   
The performance deficiency is that Susquehanna did not ensure that the plant  
referenced simulator accurately modeled the expected plant response for RPV level  
referenced simulator accurately modeled the expected plant response for RPV level  
instrumentation after a DBA LOCA, resulting in negative training of the licensed  
instrumentation after a DBA LOCA, resulting in negative training of the licensed  
operators.  
operators.  
  Analyses:  This performance deficiency is more than minor because it is associated with the Human Performance attribute of the Mitigating Systems cornerstone and affects the objective to ensure the availability, reliability, and capability of systems that respond to  
   
Analyses:  This performance deficiency is more than minor because it is associated with  
the Human Performance attribute of the Mitigating Systems cornerstone and affects the  
objective to ensure the availability, reliability, and capability of systems that respond to  
initiating events to prevent undesirable consequences.  Specifically, the incorrect  
initiating events to prevent undesirable consequences.  Specifically, the incorrect  
modeling of the Susquehanna plant referenced simulator introduces negative operator training that could affect the ability of the operators (a mitigating system) to take the appropriate actions during an actual even
modeling of the Susquehanna plant referenced simulator introduces negative operator  
t.  The simulator training conditioned the operators to expect the level instruments to be unavailable during events that cause  
training that could affect the ability of the operators (a mitigating system) to take the  
appropriate actions during an actual event.  The simulator training conditioned the  
operators to expect the level instruments to be unavailable during events that cause  
drywell temperatures to reach or exceed RPV saturation temperature.  As a result,  
drywell temperatures to reach or exceed RPV saturation temperature.  As a result,  
during an actual event, the operators could prematurely transition into the RPV flooding procedure when the RPV level instruments should be providing valid indication.  The inspectors evaluated the finding in accordance with IMC 0609, Appendix I, "Licensed  
during an actual event, the operators could prematurely transition into the RPV flooding  
Operator Requalification Significance Determination Process." The finding was  
procedure when the RPV level instruments should be providing valid indication.  The  
inspectors evaluated the finding in accordance with IMC 0609, Appendix I, Licensed  
Operator Requalification Significance Determination Process.  The finding was  
determined to be of very low safety significance (Green) because it is not related to  
determined to be of very low safety significance (Green) because it is not related to  
operator performance during requalification, it is related to simulator fidelity, and could  
operator performance during requalification, it is related to simulator fidelity, and could  
have a negative impact on operator actions.   
have a negative impact on operator actions.  
  Enclosure  
 
  15 Enforcement:  10 CFR 55.46(c)(1), "Plant Referenced Simulators," states, in part, that a plant referenced simulator must demonstrate expected plant response to normal, transient, and accident conditions.  Contrary to the above, as of January 2008, the Susquehanna plant referenced simulator did not accurately demonstrate the actual  
   
Enclosure  
   
15
Enforcement:  10 CFR 55.46(c)(1), Plant Referenced Simulators, states, in part, that a  
plant referenced simulator must demonstrate expected plant response to normal,  
transient, and accident conditions.  Contrary to the above, as of January 2008, the  
Susquehanna plant referenced simulator did not accurately demonstrate the actual  
expected plant response of the RPV water level instrumentation following a DBA LOCA,  
expected plant response of the RPV water level instrumentation following a DBA LOCA,  
which could result in negative operator training.  However, because the finding was of  
which could result in negative operator training.  However, because the finding was of  
very low safety significance (Green) and has been entered into the CAP (AR/CR 962881), this violation is being treated as an NCV, consistent with section VI.A.1 of the NRC Enforcement Policy.  (NCV 05000387/2008006-03; 05000388/2008006-03 - Failure to Accurately Model  
very low safety significance (Green) and has been entered into the CAP (AR/CR  
 
962881), this violation is being treated as an NCV, consistent with section VI.A.1 of the  
NRC Enforcement Policy.  
   
(NCV 05000387/2008006-03; 05000388/2008006-03 - Failure to Accurately Model  
the Simulator for RPV Water Level Instrumentation)  
the Simulator for RPV Water Level Instrumentation)  
    (d) Failure to Identify and Correct a Setpoint Error in the RHR and CS Operating  
Procedures
  (d)  
 
Failure to Identify and Correct a Setpoint Error in the RHR and CS Operating  
Introduction:  The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," for the failure to identify that a setpoint error in the operating procedures for safety-related systems was a CAQ, resulting in the procedures not being corrected in a timely manner.  Specifically, in February 2006, Susquehanna personnel  
Procedures  
Introduction:  The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI,  
Corrective Action, for the failure to identify that a setpoint error in the operating  
procedures for safety-related systems was a CAQ, resulting in the procedures not being  
corrected in a timely manner.  Specifically, in February 2006, Susquehanna personnel  
identified an incorrect setpoint for the low pressure injection permissive interlock in the  
identified an incorrect setpoint for the low pressure injection permissive interlock in the  
 
RHR and CS systems operating procedures and associated hard cards; however, the  
RHR and CS systems operating procedures and associated "hard cards"; however, the procedures were not revised until July 2007 due to the issue being screened as low  
procedures were not revised until July 2007 due to the issue being screened as low  
 
priority and not a condition adverse to quality (CAQ).  
priority and not a condition adverse to quality (CAQ).  
  Description:  On February 11, 2006, an AR was written to identify that the low pressure injection permissive setpoint in the RHR and CS operating procedures, and the  
   
associated operator "hard cards," was incorrect.  The correct setpoint is 420 pounds per  
Description:  On February 11, 2006, an AR was written to identify that the low pressure  
square inch gage (psig), but the procedures still had the previous setpoint of 436 psig.  The setpoint had been changed in 1999 as part of a modification.  The procedures were not revised until July 16, 2007, 17 months after the deficiency was identified in an AR.  In  
injection permissive setpoint in the RHR and CS operating procedures, and the  
associated operator hard cards, was incorrect.  The correct setpoint is 420 pounds per  
square inch gage (psig), but the procedures still had the previous setpoint of 436 psig.   
The setpoint had been changed in 1999 as part of a modification.  The procedures were  
not revised until July 16, 2007, 17 months after the deficiency was identified in an AR.  In  
addition, the inspectors noted that the setpoint in the procedures (436 psig) was not  
addition, the inspectors noted that the setpoint in the procedures (436 psig) was not  
within the allowable tolerance (407-433 psig) listed in the Susquehanna TS, Section  
within the allowable tolerance (407-433 psig) listed in the Susquehanna TS, Section  
 
3.3.5.1, Emergency Core Cooling System (ECCS) Instrumentation.  
3.3.5.1, "Emergency Core Cooling System (ECCS) Instrumentation."
 
When the AR was initiated, it was sub-classified as AR/CPG/OPS; that is, assigned to  
When the AR was initiated, it was sub-classified as AR/CPG/OPS; that is, assigned to the Central Procedures Group and identified as an Operations procedure.  It was not  
the Central Procedures Group and identified as an Operations procedure.  It was not  
recognized that deficient operating procedures for safety-related systems may be a CAQ  
recognized that deficient operating procedures for safety-related systems may be a CAQ  
and that the AR should have been classified as a Condition Report.  The affected  
and that the AR should have been classified as a Condition Report.  The affected  
section in the procedures was the verification of the response of the systems to an  
section in the procedures was the verification of the response of the systems to an  
automatic initiation signal.  For example, the Unit 1 RHR procedure OP-149-001, "RHR System," Section 2.2, noted that "No operator action is required unless an automatic action failed to occur ...  At 436 psig decreasing Reactor pressure, RHR INJ OB ISO [injection outboard isolation] HV-151-F015A & B OPEN." If the valves did not open at  
automatic initiation signal.  For example, the Unit 1 RHR procedure OP-149-001, RHR  
the specified pressure in the procedure and "hard card," the operator may have diverted their attention unnecessarily and attempted to open the valve manually, even though the
System, Section 2.2, noted that No operator action is required unless an automatic  
  Enclosure
action failed to occur ...  At 436 psig decreasing Reactor pressure, RHR INJ OB ISO  
16interlock would not have been satisfied (420 psig) and the valve would not open in accordance with the plant design. 
[injection outboard isolation] HV-151-F015A & B OPEN.  If the valves did not open at  
the specified pressure in the procedure and hard card, the operator may have diverted  
their attention unnecessarily and attempted to open the valve manually, even though the  


  The pressure switches were changed in 1999, as part of a Unit 1 plant modification (Design Change Package (DCP) 97-9075); Unit 2 switches were changed by DCP  
   
Enclosure
16
interlock would not have been satisfied (420 psig) and the valve would not open in
accordance with the plant design. 
The pressure switches were changed in 1999, as part of a Unit 1 plant modification  
(Design Change Package (DCP) 97-9075); Unit 2 switches were changed by DCP  
97-9076.  The modification replaced the existing pressure switches with Barton pressure  
97-9076.  The modification replaced the existing pressure switches with Barton pressure  
indicating switches, because of improved accuracy.  The low pressure injection  
indicating switches, because of improved accuracy.  The low pressure injection  
permissive interlock prevents the CS and RHR injection valves from opening until  
permissive interlock prevents the CS and RHR injection valves from opening until  
reactor pressure has decreased to the RHR and CS systems design pressure, to prevent over pressurization of the RHR and CS systems.  The DCP identified the specific RHR and CS operating procedures as needing to be changed.  Immediate  
reactor pressure has decreased to the RHR and CS systems design pressure, to  
prevent over pressurization of the RHR and CS systems.  The DCP identified the  
specific RHR and CS operating procedures as needing to be changed.  Immediate  
corrective actions included the initiation of a new CR to evaluate the other pending  
corrective actions included the initiation of a new CR to evaluate the other pending  
procedure changes to determine if their priority should be revised.  
procedure changes to determine if their priority should be revised.  
 
The performance deficiency involved a failure to identify and correct a CAQ, the incorrect setpoint, in a timely manner commensurate with its safety significance.  The  
The performance deficiency involved a failure to identify and correct a CAQ, the  
inspectors concluded this action was untimely because the modification process would have revised these procedures prior to the modification being accepted by operations  
incorrect setpoint, in a timely manner commensurate with its safety significance.  The  
inspectors concluded this action was untimely because the modification process would  
have revised these procedures prior to the modification being accepted by operations  
personnel.   
personnel.   
  Analysis:  The performance deficiency is more than minor because it is associated with the Procedure Quality attribute of the Mitigating Systems cornerstone and affects the  
   
Analysis:  The performance deficiency is more than minor because it is associated with  
the Procedure Quality attribute of the Mitigating Systems cornerstone and affects the  
objective to ensure the availability, reliability, and capability of systems that respond to  
objective to ensure the availability, reliability, and capability of systems that respond to  
initiating events to prevent undesirable consequences.    Specifically, the incorrect  
initiating events to prevent undesirable consequences.    Specifically, the incorrect  
setpoint reference in the procedure impacted the reliability of operator response to the event in that it could delay operator actions or result in misoperation of equipment.  The inspectors performed a review of the finding in accordance with NRC Inspection Manual  
setpoint reference in the procedure impacted the reliability of operator response to the  
Chapter (IMC) 0609, "Significance Determination Process (SDP)," Attachment 4, "Phase  
event in that it could delay operator actions or result in misoperation of equipment.  The  
1 - Initial Screening and Characterization of Findings." The inspectors determined that  
inspectors performed a review of the finding in accordance with NRC Inspection Manual  
the finding screened out as having very low safety significance (Green), because it was not a design deficiency, did not result in an actual loss of safety function, and did not screen as potentially risk significant due to external initiating events  
Chapter (IMC) 0609, Significance Determination Process (SDP), Attachment 4, Phase  
 
1 - Initial Screening and Characterization of Findings.  The inspectors determined that  
the finding screened out as having very low safety significance (Green), because it was  
not a design deficiency, did not result in an actual loss of safety function, and did not  
screen as potentially risk significant due to external initiating events  
   
   
This performance deficiency has a Cross-Cutting aspect in the area of PI&R, CAP,  
This performance deficiency has a Cross-Cutting aspect in the area of PI&R, CAP,  
because Susquehanna did not identify that a setpoint error in operating procedures for  
because Susquehanna did not identify that a setpoint error in operating procedures for  
safety-related systems was a CAQ, commensurate with its safety significance.  [P.1(a)]  
safety-related systems was a CAQ, commensurate with its safety significance.  [P.1(a)]  
  Enforcement:  10 CFR 50, Appendix B, Criterion XVI, "Corrective Action," states, in part, that conditions adverse to quality shall be promptly identified and corrected.  Contrary to  
   
Enforcement:  10 CFR 50, Appendix B, Criterion XVI, Corrective Action, states, in part,  
that conditions adverse to quality shall be promptly identified and corrected.  Contrary to  
the above, from 1999, when the pressure switches were replaced and the setpoint was  
the above, from 1999, when the pressure switches were replaced and the setpoint was  
changed, until 2006, when AR 751412 was written, Susquehanna had failed to identify that the setpoint was wrong for the low pressure injection permissive interlock in the operating procedures for RHR and CS.  Subsequently, on February 11, 2006, when  
changed, until 2006, when AR 751412 was written, Susquehanna had failed to identify  
that the setpoint was wrong for the low pressure injection permissive interlock in the  
operating procedures for RHR and CS.  Subsequently, on February 11, 2006, when  
Susquehanna personnel initiated and approved AR 751412, they failed to identify that  
Susquehanna personnel initiated and approved AR 751412, they failed to identify that  
the stated deficiency was a CAQ, which resulted in untimely corrective actions.   
the stated deficiency was a CAQ, which resulted in untimely corrective actions.   
Susquehanna considered this to be a procedure change and not a CAQ, and classified the AR as a CPG versus a CR.  As such, the procedures were not changed until July 16,   
Susquehanna considered this to be a procedure change and not a CAQ, and classified  
  Enclosure  
the AR as a CPG versus a CR.  As such, the procedures were not changed until July 16,  
  172007, 17 months after the condition was identified and eight years after the setpoint was changed in the plant.  Because this finding is of very low safety significance (Green), and  
 
was entered into the Susquehanna CAP (AR/CR 956917) this violation is being treated as a Non-Cited Violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement  
Policy.  (NCV 05000387/2008006-04; 05000388/2008006-04 - Failure to Identify and Correct  
   
Enclosure  
   
17
2007, 17 months after the condition was identified and eight years after the setpoint was  
changed in the plant.  Because this finding is of very low safety significance (Green), and  
was entered into the Susquehanna CAP (AR/CR 956917) this violation is being treated  
as a Non-Cited Violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement  
Policy.  
   
(NCV 05000387/2008006-04; 05000388/2008006-04 - Failure to Identify and Correct  
a Setpoint Error in the RHR and CS Operating Procedures)  
a Setpoint Error in the RHR and CS Operating Procedures)  
  b. Assessment of the Use of Operating Experience
 
  1. Inspection Scope
  The team reviewed a sample of operating experience (OE) issues for applicability to Susquehanna, and for the associated actions.  The documents were reviewed to ensure that underlying problems associated with the issues were appropriately considered for
resolution.  The team also reviewed how Susquehanna considered OE for applicability in causal evaluations.
Prior to the start of the inspection, the inspectors noted a potential negative trend in the
number of issues associated with reactivity management.  In accordance with the Inspection Procedure, the inspectors increased the scope of the review to determine if
there was an adverse trend in the area of reactivity management over the past five years.  The inspectors reviewed select ARs and CRs associated with the control rod
drive system, control rod problems, human performance issues, and the spent fuel pool; the inspectors review included how Susquehanna had incorporated applicable OE for
these specific systems and human performance issues into the CAP.  The inspectors interviewed selected licensee staff.
   
   
   2. Assessment
b.
  In general, OE was effectively used at the station.  The inspectors noted that OE was  
Assessment of the Use of Operating Experience
  1.
Inspection Scope
The team reviewed a sample of operating experience (OE) issues for applicability to
Susquehanna, and for the associated actions.  The documents were reviewed to ensure
that underlying problems associated with the issues were appropriately considered for
resolution.  The team also reviewed how Susquehanna considered OE for applicability in
causal evaluations.
Prior to the start of the inspection, the inspectors noted a potential negative trend in the
number of issues associated with reactivity management.  In accordance with the
Inspection Procedure, the inspectors increased the scope of the review to determine if
there was an adverse trend in the area of reactivity management over the past five
years.  The inspectors reviewed select ARs and CRs associated with the control rod
drive system, control rod problems, human performance issues, and the spent fuel pool;
the inspectors review included how Susquehanna had incorporated applicable OE for
these specific systems and human performance issues into the CAP.  The inspectors
interviewed selected licensee staff.
   2.  
Assessment  
In general, OE was effectively used at the station.  The inspectors noted that OE was  
reviewed during the causal evaluation process and incorporated, as appropriate, into the  
reviewed during the causal evaluation process and incorporated, as appropriate, into the  
development of the associated corrective actions.  The inspectors noted that OE was  
development of the associated corrective actions.  The inspectors noted that OE was  
frequently used in work packages and pre-job briefs.  The team did not identify any  
frequently used in work packages and pre-job briefs.  The team did not identify any  
significant deficiencies within the sample reviewed.  The team did not identify a negative trend nor any significant problems with the control of activities associated with reactivity management.  
significant deficiencies within the sample reviewed.  The team did not identify a negative  
trend nor any significant problems with the control of activities associated with reactivity  
management.  
  3.
Findings
No findings of significance were identified in the area of operating experience.
c.
Assessment of Self-Assessments and Audits
  1.
Inspection Scope


  3. Findings
  No findings of significance were identified in the area of operating experience.
  c. Assessment of Self-Assessments and Audits
 
Enclosure
  1. Inspection Scope
 
18
  Enclosure
The team reviewed a sample of departmental self-assessments, CAP trend reports, and  
18The team reviewed a sample of departmental self-assessments, CAP trend reports, and Quality Assurance (QA) audits, including QA's most recent audit of the CAP.  The team  
Quality Assurance (QA) audits, including QAs most recent audit of the CAP.  The team  
also reviewed the latest internal assessment of the safety culture at Susquehanna, conducted in October 2006.  The reviews were performed to determine if problems identified through these evaluations were entered into the CAP system, and whether the  
also reviewed the latest internal assessment of the safety culture at Susquehanna,  
conducted in October 2006.  The reviews were performed to determine if problems  
identified through these evaluations were entered into the CAP system, and whether the  
corrective actions were properly completed to resolve the deficiencies.  The  
corrective actions were properly completed to resolve the deficiencies.  The  
effectiveness of the audits and self-assessments was evaluated by comparing audit and  
effectiveness of the audits and self-assessments was evaluated by comparing audit and  
self-assessment results  
self-assessment results against self-revealing and NRC-identified findings, and  
against self-revealing and NRC-identified findings, and observations during the inspection.  
observations during the inspection.  
   
   
   2. Assessment
   2.  
  The team considered the quality of the audits and self-assessments to be thorough and  
Assessment  
The team considered the quality of the audits and self-assessments to be thorough and  
critical.  ARs were initiated for issues identified by QA and the self-assessments.  The  
critical.  ARs were initiated for issues identified by QA and the self-assessments.  The  
Susquehanna 2006 "Comprehensive Cultural Assessment" Report consisted of a safety culture survey and interviews.  The cultural assessment report identified some  
Susquehanna 2006 Comprehensive Cultural Assessment Report consisted of a safety  
culture survey and interviews.  The cultural assessment report identified some  
weaknesses at the station, which were entered into the CAP.  The team did not identify  
weaknesses at the station, which were entered into the CAP.  The team did not identify  
any results that were inconsistent with Susquehanna's conclusions.  
any results that were inconsistent with Susquehannas conclusions.  
 
  3. Findings
  3.  
  No findings of significance were identified in the area of audits and self-assessments.   
Findings  
No findings of significance were identified in the area of audits and self-assessments.   
d.
Assessment of Safety Conscious Work Environment
  1.
Inspection Scope
   
   
d. Assessment of Safety Conscious Work Environment
To evaluate the safety conscious work environment (SCWE) at Susquehanna, during  
    1. Inspection Scope
interviews and discussions with station personnel, the team assessed the workers  
  To evaluate the safety conscious work environment (SCWE) at Susquehanna, during interviews and discussions with station personnel, the team assessed the workers  
willingness to enter issues into the CAP and to raise safety issues to their management  
willingness to enter issues into the CAP and to raise safety issues to their management and/or to the NRC.  The inspectors also  
and/or to the NRC.  The inspectors also interviewed the Employee Concerns Program  
interviewed the Employee Concerns Program (ECP) representative to determine if employees were aware of the program and had  
(ECP) representative to determine if employees were aware of the program and had  
used it to raise concerns.  The team reviewed a sample of the ECP files to ensure that  
used it to raise concerns.  The team reviewed a sample of the ECP files to ensure that  
issues were entered into the corrective action program, as appropriate.  
issues were entered into the corrective action program, as appropriate.  
   
   
   2. Assessment
   2.  
  Based on interviews, observations of plant activities, and reviews of the ARs and ECP,  
Assessment  
Based on interviews, observations of plant activities, and reviews of the ARs and ECP,  
the inspectors determined that the site personnel were willing to raise safety issues and  
the inspectors determined that the site personnel were willing to raise safety issues and  
document them in ARs.  Individuals actively
document them in ARs.  Individuals actively utilized the AR system, as evidenced by the  
utilized the AR system, as evidenced by the number and significance of issues entered into the program.  The inspectors noted that ARs were written by a variety of personnel, from workers to managers.  ECP evaluations were thorough and appropriate actions were taken to address issues.  
number and significance of issues entered into the program.  The inspectors noted that  
ARs were written by a variety of personnel, from workers to managers.  ECP evaluations  
were thorough and appropriate actions were taken to address issues.
  3.
Findings
No findings of significance were identified related to the SCWE at Susquehanna.  


  3. Findings
  No findings of significance were identified related to the SCWE at Susquehanna.  
  Enclosure  
   
  19 4OA6 Meetings, Including Exit
Enclosure  
: On February 1, 2008, the team presented the inspection results to Mr. B. McKinney, Senior Vice President, and to other members of the Susquehanna staff, who  
   
19
4OA6 Meetings, Including Exit:
   
On February 1, 2008, the team presented the inspection results to Mr. B. McKinney,  
Senior Vice President, and to other members of the Susquehanna staff, who  
acknowledged the findings.  The team confirmed that no proprietary information  
acknowledged the findings.  The team confirmed that no proprietary information  
reviewed during the inspection was retained.  
reviewed during the inspection was retained.  
  ATTACHMENT:
   
  Supplemental Information  
ATTACHMENT: Supplemental Information  
  In addition to the documentation that the team reviewed (listed in the Attachment),  
   
In addition to the documentation that the team reviewed (listed in the Attachment),  
copies of information requests given to the licensee are in ADAMS, under accession  
copies of information requests given to the licensee are in ADAMS, under accession  
number ML080430585.   
number ML080430585.  
  Attachment  
 
A-1ATTACHMENT - SUPPLEMENTAL INFORMATION
  KEY POINTS OF CONTACT
  Licensee Personnel
   
: M. Adelizzi, Risk Engineer  
Attachment  
N. D'Angelo, Manager, Station Engineering C. Gannon, Vice President, Nuclear Operations  
A-1
ATTACHMENT - SUPPLEMENTAL INFORMATION  
KEY POINTS OF CONTACT  
Licensee Personnel:
   
M. Adelizzi, Risk Engineer  
N. DAngelo, Manager, Station Engineering  
C. Gannon, Vice President, Nuclear Operations  
T. Gorman, Project Manager, Design Engineering  
T. Gorman, Project Manager, Design Engineering  
R. Hoffman, Manager, Nuclear Fuels & Analysis  
R. Hoffman, Manager, Nuclear Fuels & Analysis  
 
B. McKinney, Chief Nuclear Officer  
B. McKinney, Chief Nuclear Officer I. Missien, Project Manager, System Engineering B. O'Rourke, Senior Engineer, Nuclear Regulatory Affairs  
I. Missien, Project Manager, System Engineering  
B. ORourke, Senior Engineer, Nuclear Regulatory Affairs  
R. Pagodin, General Manager, Nuclear Engineering  
R. Pagodin, General Manager, Nuclear Engineering  
R. Paley, General Manager, Plant Support  
R. Paley, General Manager, Plant Support  
 
A. Price, Supervisor, Corrective Action & Assessment  
A. Price, Supervisor, Corrective Action & Assessment M. Rochester, Employee Concerns Representative G. Ruppert, Manager, Maintenance  
M. Rochester, Employee Concerns Representative  
 
G. Ruppert, Manager, Maintenance  
R. Schechterly, Operating Experience Coordinator  
R. Schechterly, Operating Experience Coordinator  
R. Sgarro, Manager, Nuclear Regulatory Affairs  
R. Sgarro, Manager, Nuclear Regulatory Affairs  
M. Sleigh, Security Manager  
M. Sleigh, Security Manager  
B. Stitt, Operations Training T. Tonkinson, Supervisor, Maintenance Support D. Weller, Maintenance Foreman  
B. Stitt, Operations Training  
T. Tonkinson, Supervisor, Maintenance Support  
D. Weller, Maintenance Foreman  
L. West, Supervisor, Central Procedure Group  
L. West, Supervisor, Central Procedure Group  
 
Nuclear Regulatory Commission
Nuclear Regulatory Commission:
: M. Gray, Branch Chief, Technical Support & Assessment  
   
M. Gray, Branch Chief, Technical Support & Assessment  
F. Jaxheimer, Senior Resident Inspector  
F. Jaxheimer, Senior Resident Inspector  
 
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
  Opened and Closed
:   05000387/2008006-01  
Opened and Closed:
    
05000387/2008006-01  
05000388/2008006-01  
05000388/2008006-01  
  NCV Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an Inadequate EOP (Section 4OA2.a.3 (a))
   
  05000387/2008006-02  
NCV Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG  
Resulted in an Inadequate EOP  
(Section 4OA2.a.3 (a))
   
05000387/2008006-02  
05000388/2008006-02  
05000388/2008006-02  
  NCV Failure to Identify and Correct Inconsistencies in the Licensing Basis  
   
and the EOPs (Section 4OA2.a.3 (b))
NCV Failure to Identify and Correct Inconsistencies in the Licensing Basis  
  05000387/2008006-03  
and the EOPs  
(Section 4OA2.a.3 (b))
   
05000387/2008006-03  
05000388/2008006-03  
05000388/2008006-03  
  NCV Failure to Accurately Model the Simulator for RPV Water Level  
   
Instrumentation (Section 4OA2.a.3 (c))
NCV Failure to Accurately Model the Simulator for RPV Water Level  
  05000387/2008006-04  
Instrumentation  
(Section 4OA2.a.3 (c))
   
05000387/2008006-04  
05000388/2008006-04  
05000388/2008006-04  
  NCV Failure to Identify and Correct a Setpoint Error in the RHR and CS  
   
Operating Procedures (Section 4OA2.a.3 (d))  
NCV Failure to Identify and Correct a Setpoint Error in the RHR and CS  
  Attachment  
Operating Procedures  
  A-2LIST OF DOCUMENTS REVIEWED
(Section 4OA2.a.3 (d))
  Procedures
: BWROG EGP/SAG and Appendix B Bases, Revision 2  
Design Considerations Applicability Sheet Number 42, Emergency Plan, Revision 1 EO-000-102, RPV Control, Revision 2  
EO-000-114-1, RPV Flooding, Revision 5 EO-100-103-1, Primary Containment Control, Revision 9 EP-AD-014, Surveillance Testing of Emergency Communications Equipment, Revision 10 EP-AD-015, Review, Revision, and distribution of the SSES Emergency Plan, Revision 11  
 
Attachment  
   
A-2
LIST OF DOCUMENTS REVIEWED  
Procedures:
   
BWROG EGP/SAG and Appendix B Bases, Revision 2  
Design Considerations Applicability Sheet Number 42, Emergency Plan, Revision 1  
EO-000-102, RPV Control, Revision 2  
EO-000-114-1, RPV Flooding, Revision 5  
EO-100-103-1, Primary Containment Control, Revision 9  
EP-AD-014, Surveillance Testing of Emergency Communications Equipment, Revision 10  
EP-AD-015, Review, Revision, and distribution of the SSES Emergency Plan, Revision 11  
ME-0RF-161, Control of Fuel Pool Cleanout Activities, Revision 5  
ME-0RF-161, Control of Fuel Pool Cleanout Activities, Revision 5  
ME-0RF-163, Fuel Pool Cleanout - Energy Solutions - Dose Rate Profiling of Irradiated Hardware and Liners, Revision 4 MFP-QA-1220, Engineering Change Process Handbook, Revision 2 MI-VL-009, Operation of Leak Rate Monitors, Surge Tank Assemblies and 1035 psig Test Pumps, Revision 3 MT-AD-504, Scaffold Erection, Review and Inspection, Revisions 9 & 10  
ME-0RF-163, Fuel Pool Cleanout - Energy Solutions - Dose Rate Profiling of Irradiated  
MT-GM-018, Freeze Sealing of Piping, Revision 15 MT-GM-050, Limitorque Type SMB-000 through SMB-4 Operator Maintenance, Revision 12 NASP-QA-202, Independent Technical Review Program, Revision 2  
Hardware and Liners, Revision 4  
MFP-QA-1220, Engineering Change Process Handbook, Revision 2  
MI-VL-009, Operation of Leak Rate Monitors, Surge Tank Assemblies and 1035 psig Test  
Pumps, Revision 3  
MT-AD-504, Scaffold Erection, Review and Inspection, Revisions 9 & 10  
MT-GM-018, Freeze Sealing of Piping, Revision 15  
MT-GM-050, Limitorque Type SMB-000 through SMB-4 Operator Maintenance, Revision 12  
NASP-QA-202, Independent Technical Review Program, Revision 2  
NASP-QA-401, Internal Audits, Revision 9  
NASP-QA-401, Internal Audits, Revision 9  
NASP-QA-700, Performance Assessment Process, Revision 0  
NASP-QA-700, Performance Assessment Process, Revision 0  
NDAP-00-0109, Employee Concerns Program, Revision 10  
NDAP-00-0109, Employee Concerns Program, Revision 10  
NDAP-00-0708, Corrective Action Review Board, Revision 4 NDAP-00-0710, Station Trending Program, Revision 1 NDAP-00-0745, Self-Assessment, Benchmarking and Performance Indicators, Revision 7  
NDAP-00-0708, Corrective Action Review Board, Revision 4  
NDAP-00-0710, Station Trending Program, Revision 1  
NDAP-00-0745, Self-Assessment, Benchmarking and Performance Indicators, Revision 7  
NDAP-00-0751, Significant Operating Experience Report (SOER) Review Program, Revision 3  
NDAP-00-0751, Significant Operating Experience Report (SOER) Review Program, Revision 3  
NDAP-00-0752, Cause Analysis, Revisions 3 and 4  
NDAP-00-0752, Cause Analysis, Revisions 3 and 4  
NDAP-00-0753, Common Issue Analysis, Revision 0 NDAP-00-0778, Performance Improvement Program, Revision 2 NDAP-QA-0103, Audit Program, Revision 9  
NDAP-00-0753, Common Issue Analysis, Revision 0  
NDAP-00-0778, Performance Improvement Program, Revision 2  
NDAP-QA-0103, Audit Program, Revision 9  
NDAP-QA-0330, PSTG and Emergency Procedures, Revision 8  
NDAP-QA-0330, PSTG and Emergency Procedures, Revision 8  
NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and Writer's Guide, Revision 3 NDAP-QA-0412, Leakage Rate Test Program, Revision 10  
NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and Writers Guide, Revision 3  
NDAP-QA-0702, Action Request and Condition Report Process, Revision 20 NDAP-QA-0703, Operability Assessments and Requests for Enforcement Discretion, Revision 12 NDAP-QA-0720, Station Report Matrix and Repor
NDAP-QA-0412, Leakage Rate Test Program, Revision 10  
tability Evaluation Guidance, Revision 13 NDAP-QA-0725, Operating Experience Review Program, Revision 11  
NDAP-QA-0702, Action Request and Condition Report Process, Revision 20  
NDAP-QA-0726, 10CFR50.59 and 10CFR72.48 Implementation, Revision 10 NDAP-QA-1220, Engineering Change Process, Revision 2 NTP-QA-53.1, Susquehanna Fire Brigade Training Program, Revision 15  
NDAP-QA-0703, Operability Assessments and Requests for Enforcement Discretion,  
Revision 12  
NDAP-QA-0720, Station Report Matrix and Reportability Evaluation Guidance, Revision 13  
NDAP-QA-0725, Operating Experience Review Program, Revision 11  
NDAP-QA-0726, 10CFR50.59 and 10CFR72.48 Implementation, Revision 10  
NDAP-QA-1220, Engineering Change Process, Revision 2  
NTP-QA-53.1, Susquehanna Fire Brigade Training Program, Revision 15  
ODCM-QA-001, ODCM Introduction, Revision 3  
ODCM-QA-001, ODCM Introduction, Revision 3  
ODCM-QA-002, ODCM Review and Revision Control, Revision 4  
ODCM-QA-002, ODCM Review and Revision Control, Revision 4  
ODCM-QA-003, Effluent Monitor Setpoints, Revision 3 ODCM-QA-004, Airborne Effluent Dose Calculations, Revision 4  
ODCM-QA-003, Effluent Monitor Setpoints, Revision 3  
ODCM-QA-005, Waterborne Effluent Dose Calculation, Revision 3   
ODCM-QA-004, Airborne Effluent Dose Calculations, Revision 4  
  Attachment  
ODCM-QA-005, Waterborne Effluent Dose Calculation, Revision 3  
  A-3ODCM-QA-006, Total Dose Calculation, Revision 2  
 
ODCM-QA-007, Radioactive Waste  
Treatment Systems, Revision 2  
   
ODCM-QA-008, Radiological Environmental Monitoring Program, Revision 11 ODCM-QA-009, Dose Assessment Policy Statements, Revision 2 ON-145-004, RPV Water Level Anomaly, Revision 13  
Attachment  
   
A-3
ODCM-QA-006, Total Dose Calculation, Revision 2  
ODCM-QA-007, Radioactive Waste Treatment Systems, Revision 2  
ODCM-QA-008, Radiological Environmental Monitoring Program, Revision 11  
ODCM-QA-009, Dose Assessment Policy Statements, Revision 2  
ON-145-004, RPV Water Level Anomaly, Revision 13  
OP-024-001, Diesel Generators, Revision 49  
OP-024-001, Diesel Generators, Revision 49  
OP-024-004, Transfer and Test Mode Operations of Diesel Generator E, Revision 26  
OP-024-004, Transfer and Test Mode Operations of Diesel Generator E, Revision 26  
OP-149-001, RHR System, Revisions 31 and 32 OP-151-001, Core Spray System, Revisions 27 & 28 SE-124-007, Unit 1 Division 1 Diesel Generator LOCA LOOP Test, Revision 15  
OP-149-001, RHR System, Revisions 31 and 32  
OP-151-001, Core Spray System, Revisions 27 & 28  
SE-124-007, Unit 1 Division 1 Diesel Generator LOCA LOOP Test, Revision 15  
SE-259-044, LLRT of RHR Containment Spray Penetration Number X-39A, Revision 11  
SE-259-044, LLRT of RHR Containment Spray Penetration Number X-39A, Revision 11  
SOP-054-B03, Quarterly ESW Flow Verification Loop B, Revision 7  
SOP-054-B03, Quarterly ESW Flow Verification Loop B, Revision 7  
SSES-EPG, SSES Plant Specific Technical Guideline, Revision 9  
SSES-EPG, SSES Plant Specific Technical Guideline, Revision 9  
   
   
Audits:  666178, Corrective Action, November 2006 - February 2007  
Audits:  
   
666178, Corrective Action, November 2006 - February 2007  
667966, QA Internal Audit Report, Fuel Management, Revision 0  
667966, QA Internal Audit Report, Fuel Management, Revision 0  
691277, QA Internal Audit Report Access Authorization and Fitness for Duty, Revision 0  706249, Operations Training and Qualification Programs, May - June 2007 718607, QA Internal Audit Report, Engineering, Revision 0  
691277, QA Internal Audit Report Access Authorization and Fitness for Duty, Revision 0   
706249, Operations Training and Qualification Programs, May - June 2007  
718607, QA Internal Audit Report, Engineering, Revision 0  
744333, Operations, November - December 2007  
744333, Operations, November - December 2007  
792034, QA Internal Audit Report, Security, Revision 0  
792034, QA Internal Audit Report, Security, Revision 0  
NEIP Audit of Susquehanna Quality Assurance, June 2006  
NEIP Audit of Susquehanna Quality Assurance, June 2006  
   
   
Self-Assessments
Self-Assessments:
: 2006 Comprehensive Cultural Assessment, September - October 2006  
   
CA&A Functional Unit Excellence Plan, 1
2006 Comprehensive Cultural Assessment, September - October 2006  
st , 2 nd , and 3 rd Quarters 2007 CAA-06-01, Site Wide Self-Assessment, December 2006 CAA-06-05, Self-Assessment Program Performance, February 2006 CAA-06-08, Decrease in CR Generation Identified by Trend Report, November 2006  
CA&A Functional Unit Excellence Plan, 1st, 2nd, and 3rd Quarters 2007  
CAA-06-01, Site Wide Self-Assessment, December 2006  
CAA-06-05, Self-Assessment Program Performance, February 2006  
CAA-06-08, Decrease in CR Generation Identified by Trend Report, November 2006  
Focused Self Assessment, MOV Program Self-Assessment, October 2007  
Focused Self Assessment, MOV Program Self-Assessment, October 2007  
Maintenance Implementing Procedures Adequacy  
Maintenance Implementing Procedures Adequacy for Qualified, Inexperienced Employees,  
for Qualified, Inexperienced Employees, June 2007 Multi-Utility Joint Audit Program Initiative, March - April 2007  
June 2007  
NTG Focused Self-Assessment of Operator Training Programs, June 2007 OPS-06-02, Determine the Status of Operator Fundamentals, February 2006  
Multi-Utility Joint Audit Program Initiative, March - April 2007  
NTG Focused Self-Assessment of Operator Training Programs, June 2007  
OPS-06-02, Determine the Status of Operator Fundamentals, February 2006  
OPS-06-03, Operations Focused Se-f Assessment, July 2006  
OPS-06-03, Operations Focused Se-f Assessment, July 2006  
Pre-PI&R Focused Self-Assessment, September 2007  
Pre-PI&R Focused Self-Assessment, September 2007  
QA Organization Effectiveness Self-Assessment, October 2006 QA-06-01, Operations QA Audit Preparation Gap Analysis for QC, May - July 2006 SEC-06-01, Analyses of SSES Security Procedures and Physical Security Plan, Revision 0  
QA Organization Effectiveness Self-Assessment, October 2006  
QA-06-01, Operations QA Audit Preparation Gap Analysis for QC, May - July 2006  
SEC-06-01, Analyses of SSES Security Procedures and Physical Security Plan, Revision 0  


   
   
   
   
   
Attachment  
  Attachment  
   
  A-4Action Requests (* denotes an AR/CR generated as a result of this inspection)
A-4
: 478369 524893 542157  
Action Requests (* denotes an AR/CR generated as a result of this inspection):
   
478369  
524893  
542157  
545804  
545804  
549328  
549328  
554362 554598 555140  
554362  
554598  
555140  
555263  
555263  
555562  
555562  
557348  
557348  
565795 575128 578943  
565795  
575128  
578943  
584400  
584400  
591033  
591033  
594366 594887 595165  
594366  
594887  
595165  
604009  
604009  
604296  
604296  
610978  
610978  
615707 623914 623949  
615707  
623914  
623949  
635924  
635924  
647827  
647827  
655735 666405 668871  
655735  
666405  
668871  
669732  
669732  
677145  
677145  
687080  
687080  
688300 691108 693936  
688300  
691108  
693936  
699781  
699781  
723483  
723483  
723976 724102 724165  
723976  
724374 724467 724717 726672  
724102  
724165  
724374  
724467  
724717  
726672  
728295  
728295  
728936  
728936  
730852 730944 730947  
730852  
730944  
730947  
737236  
737236  
738555  
738555  
738575  
738575  
738634 738653 738907  
738634  
738653  
738907  
738999  
738999  
739262  
739262  
739371 739371 739386  
739371  
739371  
739386  
739419  
739419  
739579  
739579  
739625  
739625  
739713 739737 740043  
739713  
739737  
740043  
740073  
740073  
740303  
740303  
740477 740538 740658  
740477  
740538  
740658  
740668  
740668  
740723  
740723  
740802  
740802  
740804 740825 740946  
740804  
740825  
740946  
740948  
740948  
740955  
740955  
740988 741041 741321  
740988  
741457 741707 741908 741943  
741041  
741321  
741457  
741707  
741908  
741943  
742191  
742191  
742318  
742318  
742342 742427 742676  
742342  
742427  
742676  
742966  
742966  
743043  
743043  
744975  
744975  
744979 745221 745248  
744979  
745221  
745248  
745462  
745462  
745773  
745773  
746658 747077 747438  
746658  
747077  
747438  
749294  
749294  
749341  
749341  
749832  
749832  
750140 750232 751212  
750140  
750232  
751212  
751412  
751412  
751433  
751433  
751444 752341 752347  
751444  
752341  
752347  
752582  
752582  
753392  
753392  
753664  
753664  
753869 753990 755360  
753869  
753990  
755360  
756094  
756094  
756415  
756415  
756804 757530 757979  
756804  
758337 759209 759216 759827  
757530  
757979  
758337  
759209  
759216  
759827  
760281  
760281  
760526  
760526  
760526 762497 763050  
760526  
762497  
763050  
763128  
763128  
763397  
763397  
764145  
764145  
764738 764953 765421  
764738  
764953  
765421  
767566  
767566  
767567  
767567  
768301 768502 768821  
768301  
768502  
768821  
768920  
768920  
769304  
769304  
769867  
769867  
769870 770453 771319  
769870  
770453  
771319  
771876  
771876  
771961  
771961  
773046 773409 774453  
773046  
773409  
774453  
774475  
774475  
774509  
774509  
774549  
774549  
775285 775718 776112  
775285  
775718  
776112  
776171  
776171  
776769  
776769  
776918 777335 777723  
776918  
778124 779830 780144 780155  
777335  
777723  
778124  
779830  
780144  
780155  
780778  
780778  
780992  
780992  
781644 782321 782344  
781644  
782321  
782344  
783655  
783655  
784730  
784730  
784882  
784882  
784890 785561 785791  
784890  
785561  
785791  
786149  
786149  
786224  
786224  
786564 786735 786768  
786564  
786735  
786768  
787850  
787850  
788616  
788616  
788621  
788621  
788879 789971 791115  
788879  
789971  
791115  
791329  
791329  
792158  
792158  
793381 794995 795583  
793381  
794995  
795583  
796640  
796640  
797517  
797517  
799890  
799890  
802254 802539 802563  
802254  
802539  
802563  
802572  
802572  
802697  
802697  
805698 806710 809503  
805698  
809702 810391 810513 811239  
806710  
809503  
809702  
810391  
810513  
811239  
811429  
811429  
811996  
811996  
812948 813844 815268  
812948  
813844  
815268  
816097  
816097  
816710  
816710  
817720  
817720  
818082 818154 820344  
818082  
818154  
820344  
820380  
820380  
820989  
820989  
820995 821006 821064  
820995  
821006  
821064  
822996  
822996  
823908  
823908  
824522  
824522  
824895 825107 825750  
824895  
825107  
825750  
826452  
826452  
826870  
826870  
827023 827966 828626  
827023  
827966  
828626  
828744  
828744  
829065  
829065  
829502  
829502  
835002 837153 837180 839753  
835002  
837153  
837180  
839753  
841169  
841169  
841885 842663 842920  
841885  
843144 843985 845441 849935  
842663  
842920  
843144  
843985  
845441  
849935  
851918  
851918  
853358  
853358  
854681 855266 855268  
854681  
855266  
855268  
856997  
856997  
858269  
858269  
858578  
858578  
859082 859440 859794  
859082  
859440  
859794  
859839  
859839  
860299  
860299  
860551 861162 861366  
860551  
861162  
861366  
861415  
861415  
862474  
862474  
864090  
864090  
865286 865423 865804  
865286  
865423  
865804  
865924  
865924  
866930  
866930  
867534 867747 867881  
867534  
867747  
867881  
868251  
868251  
868259  
868259  
868828  
868828  
868874 869819 869824  
868874  
869819  
869824  
870968  
870968  
871013  
871013  
872039 872056 873026  
872039  
873683 873741 873919 874227  
872056  
873026  
873683  
873741  
873919  
874227  
875597  
875597  
875976  
875976  
876021 876427 877419  
876021  
876427  
877419  
877727  
877727  
877743  
877743  
878165  
878165  
878326 879080 879847  
878326  
879080  
879847  
880331  
880331  
880573  
880573  
880702 880806 881210  
880702  
880806  
881210  
881219  
881219  
881225  
881225  
881236  
881236  
882318 883987 886209  
882318  
883987  
886209  
887048  
887048  
887067  
887067  
888310 889683 889966  
888310  
889683  
889966  
891288  
891288  
891733  
891733  
891795  
891795  
892142 892152 892528  
892142  
892152  
892528  
893090  
893090  
893157  
893157  
893290 895147 896455  
893290  
896505 896685 897250 898909  
895147  
896455  
896505  
896685  
897250  
898909  
899429  
899429  
900301  
900301  
900720 901262 903439  
900720  
901262  
903439  
904689  
904689  
908163  
908163  
911601  
911601  
912213 912476 915167  
912213  
912476  
915167  
915620  
915620  
916453  
916453  
916463 916873 917196  
916463  
916873  
917196  
918392  
918392  
918549  
918549  
919470  
919470  
927046 928515 929461  
927046  
928515  
929461  
930075  
930075  
930571  
930571  
931113 932590 936060  
931113  
932590  
936060  
936250  
936250  
936370  
936370  
936631  
936631  
937123 938054 938698  
937123  
938054  
938698  
938722  
938722  
939516  
939516  
939780 941290 941401  
939780  
941626 941677 941810 947160  
941290  
941401  
941626  
941677  
941810  
947160  
954950*  
954950*  
954970*  
954970*  
954972* 954975* 954990*  
954972*  
954975*  
954990*  
955072*  
955072*  
955073*  
955073*  
955111*  
955111*  
955130* 955150* 955151*  
955130*  
955150*  
955151*  
955761*  
955761*  
955780*  
955780*  
956339* 956344* 956431*  
956339*  
956344*  
956431*  
956696*  
956696*  
956914*  
956914*  
956917*  
956917*  
957319* 957484* 957637*  
957319*  
957484*  
957637*  
958769*  
958769*  
959670*  
959670*  
961655 962390 962881*  
961655  
962390  
962881*  
963061*  
963061*  
963065*  
963065*  
963698*  
963698*  
963861* 964512* 964514*  
963861*  
964512*  
964514*  
964836*  
964836*  
965167*    
965167*  
  Attachment  
  A-5 Maintenance Work Requests (SPWO)
: 099065 099115 099120  
099259 099364 448229 473889  
 
570758 766396 766401 766406  
766411 766413 766416 766496  
767283 767284 767490 767506  
Attachment  
767532 768234 768618 818282  
   
862503 862569 862578 866262  
A-5
866284  Non-Cited Violations and Findings Reviewed
Maintenance Work Requests (SPWO):
: NCV 2005005-01, Inadequate FME Exclusion Procedural Instructions Associated with EDG  
   
Work FIN 2005009-01, Fire Brigade Drill Program Not Consistent with Regulatory Guidance and  
099065  
Industry Standards NCV 2006002-01, Equipment Hatch Plugs are Not Watertight as Indicated in FSAR FIN 2006002-02, Incomplete Corrective Actions Contribute to CRD Flow Control Failure NCV 2006003-01, Inadequate Procedures Resulted in Motor Operated Valve Failures  
099115  
NCV 2006003-02, Failure to Identify Material Degradation which Resulted in the Failure of the "C" ESW Pump Breaker NCV 2006003-03, Inadequate Procedure Results in Elevated Reactor Coolant System Leakage NCV 2006003-04, Inadequate Design Review of PRDNMS Modification Resulted in a Reactor  
099120  
Scram NCV 2006003-05, Ineffective Corrective Actions to Assure Training and Qualification of Workers as Required by 10CFR50, Appendix B, Criterion XVI NCV 2006004-01, Inadequate Risk Assessment  
099259  
099364  
448229  
473889  
570758  
766396  
766401  
766406  
766411  
766413  
766416  
766496  
767283  
767284  
767490  
767506  
767532  
768234  
768618  
818282  
862503  
862569  
862578  
866262  
866284  
   
Non-Cited Violations and Findings Reviewed:
   
NCV 2005005-01, Inadequate FME Exclusion Procedural Instructions Associated with EDG  
Work  
FIN 2005009-01, Fire Brigade Drill Program Not Consistent with Regulatory Guidance and  
Industry Standards  
NCV 2006002-01, Equipment Hatch Plugs are Not Watertight as Indicated in FSAR  
FIN 2006002-02, Incomplete Corrective Actions Contribute to CRD Flow Control Failure  
NCV 2006003-01, Inadequate Procedures Resulted in Motor Operated Valve Failures  
NCV 2006003-02, Failure to Identify Material Degradation which Resulted in the Failure of the  
C ESW Pump Breaker  
NCV 2006003-03, Inadequate Procedure Results in Elevated Reactor Coolant System Leakage  
NCV 2006003-04, Inadequate Design Review of PRDNMS Modification Resulted in a Reactor  
Scram  
NCV 2006003-05, Ineffective Corrective Actions to Assure Training and Qualification of Workers  
as Required by 10CFR50, Appendix B, Criterion XVI  
NCV 2006004-01, Inadequate Risk Assessment  
NCV 2006005-01, Inadequate Work Instructions for the Disassembly and Inspection of Check  
NCV 2006005-01, Inadequate Work Instructions for the Disassembly and Inspection of Check  
Valves NCV 2006005-02, Inadequate Evaluation of EPA Breaker Failures  
Valves  
NCV 2006006-01, Failure to Identify Scaffolding that Affected the Safety-Related RHR Discharge Pressure Instrument Tubing Input to ADS NCV 2006009-01, Safeguards Information Licensee Identified NCV 2007002, U2 Div II Core Spray Pump Room (a High Radiation Area) Was Not Posted and Was Open Licensee Identified NCV 2007002, U1 HPCI Failed a Surveillance Due to the Failure to Perform  
NCV 2006005-02, Inadequate Evaluation of EPA Breaker Failures  
Preventive Maintenance NCV 2007003-01, Failure to Take Timely Corrective Actions for an "E" EDG Jacket Water Leak  
NCV 2006006-01, Failure to Identify Scaffolding that Affected the Safety-Related RHR  
Discharge Pressure Instrument Tubing Input to ADS  
NCV 2006009-01, Safeguards Information  
Licensee Identified NCV 2007002, U2 Div II Core Spray Pump Room (a High Radiation Area)  
Was Not Posted and Was Open  
Licensee Identified NCV 2007002, U1 HPCI Failed a Surveillance Due to the Failure to Perform  
Preventive Maintenance  
NCV 2007003-01, Failure to Take Timely Corrective Actions for an E EDG Jacket Water Leak  
FIN 2007003-02, Failure to Maintain Occupational Radiation Exposure ALARA during Reactor  
FIN 2007003-02, Failure to Maintain Occupational Radiation Exposure ALARA during Reactor  
Water Cleanup Pipe Replacement Activities FIN 2007003-03, Failure to Maintain Occupational Radiation Exposure ALARA during Outage ISI of Reactor Pressure Vessel NCV 2007003-04, Violation of 10CFR71.5 for Inadequately Secured Transport of Condensate Pump Motors NCV 2007003-05, Violation of 10CFR71.5 for Inadequately Accounting for Activity in a Shipment of Irradiated Fuel Channels Licensee Identified NCV 2007003, U2 Reactor Building HRA Postings and Boundary Moved  
Water Cleanup Pipe Replacement Activities  
without Permission of RP NCV 2007007-01, Inoperable ESSW Pump-House Ventilation Lineup NCV 2007007-02, Failure to Use "E" EDG Procedure  
FIN 2007003-03, Failure to Maintain Occupational Radiation Exposure ALARA during Outage  
 
ISI of Reactor Pressure Vessel  
  Attachment  
NCV 2007003-04, Violation of 10CFR71.5 for Inadequately Secured Transport of Condensate  
  A-6 Miscellaneous
Pump Motors  
: 5059-01-2356, 50.59 Screen of Specification C-1056, Long Term Scaffolding, Revision 4 CP067, Corrective Action Program - Evaluation & Resolution, Revision 8 (Lesson Plan & Student Material) CP068, Managing the Corrective Action Process, Revision 2 (Lesson Plan & Student Material)  
NCV 2007003-05, Violation of 10CFR71.5 for Inadequately Accounting for Activity in a  
Shipment of Irradiated Fuel Channels  
Licensee Identified NCV 2007003, U2 Reactor Building HRA Postings and Boundary Moved  
without Permission of RP  
NCV 2007007-01, Inoperable ESSW Pump-House Ventilation Lineup  
NCV 2007007-02, Failure to Use E EDG Procedure  
 
Attachment  
   
A-6
Miscellaneous:
   
5059-01-2356, 50.59 Screen of Specification C-1056, Long Term Scaffolding, Revision 4  
CP067, Corrective Action Program - Evaluation & Resolution, Revision 8  
(Lesson Plan & Student Material)  
CP068, Managing the Corrective Action Process, Revision 2 (Lesson Plan & Student Material)  
Daily CR Screening Team Package  
Daily CR Screening Team Package  
Design Verification Checklist for SCN 6 for Specification C-1056, dated April 27, 2001 EC-059-1024, Design Requirements for and Evaluation of Potential Secondary Containment  
Design Verification Checklist for SCN 6 for Specification C-1056, dated April 27, 2001  
Bypass Leakage Pathways, Revision 4 EC-RADN-1029, SSES Design Basis LOCA Dose
EC-059-1024, Design Requirements for and Evaluation of Potential Secondary Containment  
Consequence Evaluation for Containment Bypass Leakage Including the Effects of Suppression Pool Scrubbing, Revision 1 EC-SIMU-1001, Evaluation of Simulator Level Instrument Response to Large LOCA, dated May 4, 1994 Engineering Specification C-1056, Erection of Scaffolding in Safety-Related Areas, Revision 4 EWR #MIS-85-0460, Design Inputs and Considerations Checklist for Specification C-1056, Revision 2 Hot Box Item 08-01, Reactor Water Instrumentation Response during DBA LOCA, dated  
Bypass Leakage Pathways, Revision 4  
January 31, 2008 IEEE Standard 497-2002, IEEE Standard Criteria for Accident Monitoring Instrumentation, dated September 30, 2002 Long Term Scaffold Log, dated January 16, 2008  
EC-RADN-1029, SSES Design Basis LOCA Dose Consequence Evaluation for Containment  
Bypass Leakage Including the Effects of Suppression Pool Scrubbing, Revision 1  
EC-SIMU-1001, Evaluation of Simulator Level Instrument Response to Large LOCA, dated  
May 4, 1994  
Engineering Specification C-1056, Erection of Scaffolding in Safety-Related Areas, Revision 4  
EWR #MIS-85-0460, Design Inputs and Considerations Checklist for Specification C-1056,  
Revision 2  
Hot Box Item 08-01, Reactor Water Instrumentation Response during DBA LOCA, dated  
January 31, 2008  
IEEE Standard 497-2002, IEEE Standard Criteria for Accident Monitoring Instrumentation, dated  
September 30, 2002  
Long Term Scaffold Log, dated January 16, 2008  
No Degraded Condition Response to OFR 963310, dated January 30, 2008  
No Degraded Condition Response to OFR 963310, dated January 30, 2008  
NRC Information Notice 2007-29, Temporary Scaffolding Affects Operability of Safety-Related  
NRC Information Notice 2007-29, Temporary Scaffolding Affects Operability of Safety-Related  
Equipment, dated September 17, 2007 NRC Inspection Procedure 42001, Emergency Operating Procedures, dated June 28, 1991 NRC Regulatory Guide 1.97, Instrumentation for Light-Water-Cooled Nuclear Power Plants to Assess Plant and Environs Conditions During and Following an Accident, Revision 2 NRC Regulatory Issue Summary 2005-20, Information to Licensees Regarding Two NRC Inspection Manual Sections on Resolution of Degraded and Nonconforming Conditions and  
Equipment, dated September 17, 2007  
on Operability NRC Regulatory Issue Summary 2007-21, Adherence to Licensed Power Limits, dated August 23, 2007 NEDE-24801, Review of BWR Reactor Vessel Water Level Measurement, April 1980  
NRC Inspection Procedure 42001, Emergency Operating Procedures, dated June 28, 1991  
NRC Regulatory Guide 1.97, Instrumentation for Light-Water-Cooled Nuclear Power Plants to  
Assess Plant and Environs Conditions During and Following an Accident, Revision 2  
NRC Regulatory Issue Summary 2005-20, Information to Licensees Regarding Two NRC  
Inspection Manual Sections on Resolution of Degraded and Nonconforming Conditions and  
on Operability  
NRC Regulatory Issue Summary 2007-21, Adherence to Licensed Power Limits, dated  
August 23, 2007  
NEDE-24801, Review of BWR Reactor Vessel Water Level Measurement, April 1980  
NEDO-24708A, Additional Information Required for NRC Staff Generic Report on Boiling Water  
NEDO-24708A, Additional Information Required for NRC Staff Generic Report on Boiling Water  
Reactors, Revision 1 Operational Policy Statement (OPS) - 5, Deficiency Control System, Revision 13 Operations Monthly Performance Indicators, December 2007  
Reactors, Revision 1  
 
Operational Policy Statement (OPS) - 5, Deficiency Control System, Revision 13  
Operations Monthly Performance Indicators, December 2007  
Operations Quality Assurance Manual, dated December 13, 2007  
Operations Quality Assurance Manual, dated December 13, 2007  
OPEX Daily Report, January 29, 2008  
OPEX Daily Report, January 29, 2008  
Plant Modification Package - DCP/ECO #97-9075, Unit 1 Core Spray/RHR/LPCI Pressure  
Plant Modification Package - DCP/ECO #97-9075, Unit 1 Core Spray/RHR/LPCI Pressure  
Switch Replacement, Revision 1 PL-NF-02-07, Channel Management Action Plan, Revision 28  
Switch Replacement, Revision 1  
PL-NF-02-07, Channel Management Action Plan, Revision 28  
Regulatory Guide 1.97, Criteria for Accident Monitoring Instrumentation, Revision 4  
Regulatory Guide 1.97, Criteria for Accident Monitoring Instrumentation, Revision 4  
Specification Change Notice #6 for C-1056, Revision 3  
Specification Change Notice #6 for C-1056, Revision 3  
Temporary Scaffold Log, dated January 15, 2008 Unit 1 & 2, Control Rod Drive Hydraulics System Health Report, May - August 2007 Unit 1, RHR Residual Heat Removal System Health Report, September - December 2007   
Temporary Scaffold Log, dated January 15, 2008  
  Attachment  
Unit 1 & 2, Control Rod Drive Hydraulics System Health Report, May - August 2007  
  A-7LIST OF ACRONYMS
Unit 1, RHR Residual Heat Removal System Health Report, September - December 2007  
  ACE Apparent Cause Evaluation AR Action Request BWROG Boiling Water Reactor Owners' Group  
 
CAP Corrective Action Program  
CAQ Condition Adverse to Quality  
   
CARB Corrective Action Review Board CFR Code of Federal Regulations CPG Central Procedure Group  
Attachment  
CR Condition Report  
   
CS Core Spray  
A-7
DBA Design Basis Accident  
LIST OF ACRONYMS  
DCP Design Change Package ECCS Emergency Core Cooling System ECP Employee Concerns Program  
EOP Emergency Operating Procedures  
ACE  
EPG/SAG Emergency Procedure Guidelines / Severe Accident Guidelines EPU Extended Power Uprate FSAR Final Safety Analysis Report IMC NRC Inspection Manual Chapter  
Apparent Cause Evaluation  
LOCA Loss of Coolant Accident  
AR  
NCV Non-Cited Violation  
Action Request  
NRC Nuclear Regulatory Commission  
BWROG  
OE Operating Experience PAM Post-Accident Monitoring PI&R Problem Identification and Resolution  
Boiling Water Reactor Owners Group  
psig pounds per square inch  
CAP  
PSTG Plant Specific Technical Guidelines  
Corrective Action Program  
QA Quality Assurance RCA Root Cause Analysis RHR Residual Heat Removal  
CAQ  
ROP Reactor Oversight Program  
Condition Adverse to Quality  
RPV Reactor Pressure Vessel  
CARB  
SCWE Safety Conscious Work Environment  
Corrective Action Review Board  
SDP Significance Determination Process TS Technical Specifications
CFR  
Code of Federal Regulations  
CPG  
Central Procedure Group  
CR  
Condition Report  
CS  
Core Spray  
DBA  
Design Basis Accident  
DCP  
Design Change Package  
ECCS  
Emergency Core Cooling System  
ECP  
Employee Concerns Program  
EOP  
Emergency Operating Procedures  
EPG/SAG  
Emergency Procedure Guidelines / Severe Accident Guidelines  
EPU  
Extended Power Uprate  
FSAR  
Final Safety Analysis Report  
IMC  
NRC Inspection Manual Chapter  
LOCA  
Loss of Coolant Accident  
NCV  
Non-Cited Violation  
NRC  
Nuclear Regulatory Commission  
OE  
Operating Experience  
PAM  
Post-Accident Monitoring  
PI&R  
Problem Identification and Resolution  
psig  
pounds per square inch  
PSTG  
Plant Specific Technical Guidelines  
QA  
Quality Assurance  
RCA  
Root Cause Analysis  
RHR  
Residual Heat Removal  
ROP  
Reactor Oversight Program  
RPV  
Reactor Pressure Vessel  
SCWE  
Safety Conscious Work Environment  
SDP  
Significance Determination Process  
TS  
Technical Specifications
}}
}}

Latest revision as of 17:40, 14 January 2025

IR 05000387-08-006, 05000388-08-006, on 01/14/2008 - 02/01/2008, Susquehanna Steam Electric Station; Biennial Baseline Inspection of He Identification and Resolution of Problems; Corrective Action Program, Simulator Fidelity, and Procedure
ML080770308
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 03/17/2008
From: Mel Gray
Division Reactor Projects I
To: Mckinney B
Susquehanna
Gray M, RI/DRP/TSAB/610-337-5209
References
IR-08-006
Download: ML080770308 (29)


See also: IR 05000387/2008006

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406-1415

March 17, 2008

Mr. Britt T. McKinney

Senior Vice President and Chief Nuclear Officer

PPL Susquehanna, LLC

769 Salem Blvd. - NUCSB3

Berwick, PA 18603-0467

SUBJECT:

SUSQUEHANNA STEAM ELECTRIC STATION, UNITS 1 AND 2

PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION

INSPECTION REPORTS NOS. 05000387/2008006; 05000388/2008006

Dear Mr. McKinney:

On February 1, 2008, the US Nuclear Regulatory Commission (NRC) completed a team

inspection at the Susquehanna Steam Electric Station. The enclosed inspection report

documents the inspection results, which were discussed on February 1, 2008, with you and

members of your staff.

This inspection was an examination of activities conducted under your license as they relate to

the identification and resolution of problems, and compliance with the Commission=s rules and

regulations and the conditions of your license. Within these areas, the inspection involved

examination of selected procedures and representative records, observations of activities, and

interviews with personnel.

On the basis of the sample selected for review, the team concluded that the implementation of

the corrective action program (CAP) was adequate in that personnel identified issues at a low

threshold; generally screened and prioritized issues in a timely manner; evaluated the issues

commensurate with their safety significance; and implemented corrective actions in a timely

manner commensurate with the safety significance.

The team identified four findings of very low safety significance (Green). These findings were

determined to involve violations of regulatory requirements. However, because each of the

violations was of very low safety significance (Green) and because they were entered into your

corrective action program, the NRC is treating these as Non-Cited Violations (NCVs), in

accordance with Section VI.A.1 of the NRC=s Enforcement Policy. If you contest any NCV in

this report, you should provide a response within 30 days of the date of this inspection report,

with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document

Control Desk, Washington DC, 20555-0001, with copies to the Regional Administrator, Region I;

B. McKinney

2

the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC,

20555-0001; and the NRC Resident Inspector at the Susquehanna facility.

In accordance with 10 CFR 2.390 of the NRC=s ARules of Practice,@ a copy of this letter and its

enclosure, and your response (if any), will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC=s document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mel Gray, Chief

Technical Support & Assessment Branch

Division of Reactor Projects

Docket Nos. 50-387, 50-388

License Nos. NPF-14; NPF-22

Enclosure:

Inspection Report Nos. 05000387/2008006; 05000388/2008006

w/ Attachment: Supplemental Information

cc w/encl:

C. Gannon, Vice President, Nuclear Operations

R. Paley, General Manager, Plant Support

R. Pagodin, General Manager, Nuclear Engineering

R. Sgarro, Manager, Nuclear Regulatory Affairs

Supervisor, Nuclear Regulatory Affairs

M. Crowthers, Supervising Engineer, Nuclear Regulatory Affairs

R. Peal, Mgr, Training, Susquehanna

Manager, Quality Assurance

J. Scopelliti, Community Relations Manager, Susquehanna

B. Snapp, Esq., Associate General Counsel, PPL Services Corporation

Supervisor - Document Control Services

R. Osborne, Allegheny Electric Cooperative, Inc.

D. Allard, Dir, PA Dept of Environmental Protection

Board of Supervisors, Salem Township

J. Johnsrud, National Energy Committee, Sierra Club

E. Epstein, TMI-Alert (TMIA)

J. Powers, Dir, PA Office of Homeland Security

R. French, Dir, PA Emergency Management Agency

Enclosure

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No:

50-387, 50-388

License No:

NPF-14, NPF-22

Report No:

05000387/2008006, 05000388/2008006

Licensee:

PPL Susquehanna, LLC

Facility:

Susquehanna Steam Electric Station, Units 1 and 2

Location:

769 Salem Boulevard - NUCSB3

Berwick, PA 18603-0467

Dates:

January 14 - February 1, 2008

Team Leader:

B. Norris, Senior Project Engineer, Division of Reactor Projects

Inspectors:

F. Arner, Senior Reactor Inspector, Division of Reactor Safety

R. Fuhrmeister, Senior Project Engineer, Division of Reactor Projects

G. Ottenberg, Resident Inspector, Division of Reactor Projects

J. Bream, Reactor Engineer, Division of Reactor Projects

R. McKinley, Operations Examiner, Division of Reactor Safety

Approved by:

Mel Gray, Chief

Technical Support & Assessment Branch

Division of Reactor Projects

Enclosure

2

SUMMARY OF FINDINGS

IR 05000387/2008-006, 05000388/2008-006; 01/14/2008 - 02/01/2008; Susquehanna Steam

Electric Station; Biennial Baseline Inspection of the Identification and Resolution of Problems;

Corrective Action Program, Simulator Fidelity, and Procedure Quality.

This team inspection was performed by five NRC regional inspectors and one resident

inspector. Four findings of very low safety significance (Green) were identified during this

inspection and determined to be Non-Cited Violations (NCVs). The significance of most findings

is indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter

(IMC) 0609, ASignificance Determination Process@ (SDP). The NRC=s program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649, AReactor

Oversight Process,@ Revision 4, dated December 2006.

Identification and Resolution of Problems

The team concluded that the implementation of the corrective action program (CAP) at

Susquehanna was adequate in that personnel identified issues at a low threshold and used a

single entry-point system to document the problems by the initiation of an Action Request (AR).

About 20 percent of the ARs were considered to be conditions adverse to quality (CAQ) and

sub-classified as a Condition Report (CR). However, the team identified several ARs that

should have been classified as CAQs; as a result, CRs were not written and corrective actions

were not timely. The team identified two findings of very low significance related to the AR

process that had current performance cross-cutting aspects in problem identification because

the issues were not categorized commensurate with their safety significance. Notwithstanding

these two findings, the team concluded that in general Susquehanna personnel screened and

prioritized CRs in a timely manner using established criteria.

The team also concluded that Susquehanna personnel properly evaluated the issues

commensurate with their safety significance; and generally implemented corrective actions in a

timely manner, commensurate with the safety significance. The team noted that Susquehanna

reviewed and applied industry operating experience lessons learned. Audits and self-

assessments added value to the corrective action process. On the basis of interviews

conducted during the inspection, workers at the site expressed freedom to enter safety

concerns into the CAP.

Enclosure

3

a. NRC Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

C

Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, because, in the 1990s, Susquehanna failed to

adequately evaluate a deviation from the Boiling Water Reactor Owners Group

Emergency Procedure Guidelines / Severe Accident Guidelines (BWROG EPG/SAG),

which resulted in one of the emergency operating procedures (EOPs) being inadequate.

Specifically, Caution #1 in the BWROG EPG/SAG warned the operators that reactor

pressure vessel (RPV) level instrumentation may be unreliable if the drywell

temperatures exceeded RPV saturation temperature. The purpose of the Caution was

to give the operators a chance to evaluate the validity of the RPV level instrumentation

to avoid premature entry into the RPV flooding contingency procedure. Susquehanna

did not adequately evaluate the deviation, and the Susquehanna EOPs did not use a

Caution statement; but instead, changed the caution to a procedural step, which directed

the operators to transition directly to the RPV flooding procedure.

The performance deficiency is more than minor because it is associated with the

Procedure Quality attribute of the Mitigating Systems cornerstone and affects the

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the EOP could have

directed entry into the RPV flooding procedure unnecessarily which would have

restricted the use of suppression pool cooling and required other actions that would have

complicated the operators response to the event. The finding was determined to be of

very low safety significance because it was not a design deficiency, did not result in an

actual loss of safety function, and did not screen as potentially risk significant due to

external initiating events. (Section 4OA2.a.3 (a))

C

Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion

XVI, Corrective Action, for the failure to identify that an inconsistency between the

procedures and the design basis for suppression pool (SP) cooling was a condition

adverse to quality (CAQ), which resulted in corrective actions not being taken in a timely

manner. Specifically, in January 2006, a Condition Report (CR) identified an

inconsistency between an assumption in the Final Safety Analysis Report (FSAR) for the

design basis accident and the emergency operating procedures (EOPs) regarding the

timing for the implementation of SP cooling. At the time of the inspection, the

inconsistency had not been resolved because Susquehanna did not recognize that it

impacted current plant operations. This performance deficiency has a cross-cutting

aspect in the area of Problem Identification and Resolution, Corrective Action Program,

because Susquehanna did not identify that the inconsistency documented in the CR

should have been categorized as a CAQ, commensurate with its safety significance.

P.1(a)

The performance deficiency is more than minor because it is associated with the Design

Control attribute of Mitigating Systems and affects the cornerstone objective to ensure

the availability, reliability, and capability of systems that respond to initiating events to

Enclosure

4

prevent undesirable consequences. Specifically, the EOPs provided direction that,

under some accident conditions, would affect the availability and/or capability of the SP

cooling system to perform its safety function. The finding screened out as having very

low safety significance because it was not a design deficiency, did not result in an actual

loss of safety function, and did not screen as potentially risk significant due to external

initiating events. (Section 4OA2.a.3 (b))

C

Green: The NRC identified a Non-Cited Violation of 10 CFR 55.46(c)(1), Plant

Referenced Simulators, because the Susquehanna simulator did not accurately model

reactor pressure vessel (RPV) level instrumentation following a design basis accident

loss of coolant accident (DBA LOCA). Specifically, an analysis performed in 1994 to

determine if the observed simulator response during a large break LOCA was consistent

with the expected plant response, was based on an overly conservative assumption that

the drywell would experience superheated conditions, which would cause RPV water

level instrumentation reference leg flashing and a subsequent loss of all RPV level

indication. The expected plant response, as stated in the analysis, was incorrect; in that

a LOCA would not always cause a loss of all RPV level instruments. As a result, the

simulator modeling was incorrect.

The performance deficiency is more than minor because it is associated with the Human

Performance attribute of Mitigating Systems and affects the cornerstone objective to

ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, the modeling of the

Susquehanna simulator introduced negative operator training that could affect the ability

of the operators (a mitigating system) to take the appropriate actions during an actual

event. The finding was determined to be of very low safety significance because it is not

related to operator performance during requalification, it is related to simulator fidelity,

and it could have a negative impact on operator actions. (Section 4OA2.a.3 (c))

C

Green: The NRC identified a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion

XVI, Corrective Action, for the failure to identify that a setpoint error in the operating

procedures for safety-related systems was a condition adverse to quality (CAQ),

resulting in the procedures not being corrected in a timely manner. The setpoint for the

low pressure injection permissive interlock in the RHR and CS systems had been

changed in 1999 as part of a modification. However, the setpoint was not changed in

the system operating procedures and operator aids. When this issue was identified by

Susquehanna staff in 2006, the setpoint error in the procedure was not screened as a

CAQ, which resulted in the procedures not being revised for 17 months after the issue

was identified in an Action Report. This performance deficiency has a cross-cutting

aspect in the area of Problem Identification and Resolution, Corrective Action Program,

because Susquehanna did not identify that a setpoint error in operating procedures for

safety-related systems was a CAQ, commensurate with its safety significance. P.1(a)

The performance deficiency is more than minor because it is associated with the

Procedure Quality attribute of Mitigating Systems and affects the cornerstone objective

to ensure the availability, reliability, and capability of systems that respond to initiating

events to prevent undesirable consequences. Specifically, the incorrect setpoint

Enclosure

5

reference in the procedure impacted the reliability of operator response to the event in

that it could delay operator actions or result in misoperation of equipment. The finding

screened out as having very low safety significance because it was not a design

deficiency, did not result in an actual loss of safety function, and did not screen as

potentially risk significant due to external initiating events. (Section 4OA2.a.3 (e))

b. Licensee-Identified Violations

None.

Enclosure

6

REPORT DETAILS

4.

OTHER ACTIVITIES (OA)

4OA2 Problem Identification and Resolution (PI&R) (Biennial - IP 71152B)

a.

Assessment of the Corrective Action Program

1.

Inspection Scope

The inspection team reviewed the procedures describing the corrective action program

(CAP) at the Susquehanna Steam Electric Station. Susquehanna used a single-point

entry system and identified problems by the initiation of an Action Request (AR). The

AR would then be sub-classified depending on the information provided; for example, as

WO for a maintenance Work Order, as CPG for assignment to the Central Procedure

Group, or as CR for a Condition Report. ARs were sub-classified as CRs for conditions

adverse to quality (CAQ), such as plant equipment deficiencies, industrial or radiological

safety concerns, or other significant issues. The CRs were subsequently screened for

operability and reportability, categorized by significance (1 to 3), assigned a level of

evaluation, and issued for resolution.

The team reviewed CRs selected across the seven cornerstones of safety in the NRC=s

Reactor Oversight Process (ROP) to determine if problems were being properly

identified, characterized, and entered into the CAP for evaluation and resolution. The

team selected items from the maintenance, operations, engineering, emergency

preparedness, physical security, radiation safety, training, and oversight programs to

ensure that Susquehanna was appropriately considering problems identified in each

functional area. The team used this information to select a risk-informed sample of CRs

that had been issued since the last NRC PI&R inspection, which was conducted in

February 2006.

The team selected ARs from other sub-classifications, to determine if Susquehanna had

appropriately classified these items as not needing to be a CR. The team also reviewed

operator log entries, control room deficiency lists, operator work-around lists, operability

determinations, engineering system health reports, completed surveillance tests, and

current temporary configuration change packages. In addition, the team interviewed

plant staff and management to determine their understanding of and involvement with

the CAP at Susquehanna. The CRs, and other documents reviewed, and the key

personnel contacted, are listed in the Attachment to this report.

The team considered risk insights from the NRC=s and Susquehanna=s risk analyses to

focus the sample selection and plant tours on risk-significant components. The team

determined that the five highest risk-significant systems at Susquehanna were

emergency service water, emergency diesel generators, residual heat removal service

water, station black-out diesel generator, and reactor core isolation cooling. For the

risk-significant systems, the team reviewed a sample of the applicable system health

Enclosure

7

reports, work requests and engineering documents, plant log entries, and results from

surveillance tests and maintenance tasks.

The team reviewed CRs to assess whether Susquehanna adequately evaluated and

prioritized the identified problems. The CRs reviewed encompassed the full range of

Susquehanna=s causal evaluations, including root cause analyses (RCA - to determine

the cause and prevent recurrence), apparent cause evaluations (ACE - to obtain a basic

understanding of the cause), and evaluations (to determine if a problem exists). The

review included the appropriateness of the assigned significance, the scope and depth

of the causal analysis, and the timeliness of the resolutions. For significant conditions

adverse to quality, the team reviewed the effectiveness of the corrective actions to

prevent recurrence. The team observed meetings of the CR Screening Team - in which

Susquehanna personnel reviewed new CRs for prioritization, and evaluated preliminary

corrective action assignments, analyses, and plans. The team also attended meetings

of the Corrective Action Review Board (CARB) - where senior managers reviewed

selected evaluations, effectiveness reviews, and extension requests.

The team reviewed equipment operability determinations, reportability assessments, and

extent-of-condition reviews for selected problems. The team assessed the backlog of

corrective actions in the maintenance, engineering, and operations departments, to

determine, individually and collectively, if there was an increased risk due to delays in

implementation of corrective actions. The team further reviewed equipment

performance results and assessments documented in completed surveillance

procedures, operator log entries, and trend data to determine whether the evaluations

were technically adequate to identify degrading or non-conforming equipment.

The team reviewed the corrective actions associated with selected CRs to determine if

the actions addressed the identified causes of the problems. The team reviewed CRs

for significant repetitive problems to determine if previous corrective actions were

effective. The team also reviewed Susquehanna=s timeliness in implementing corrective

actions. The team reviewed the CRs associated with selected non-cited violations

(NCVs) and findings to determine if Susquehanna properly evaluated and resolved these

issues.

2.

Assessment

(a)

Identification of Issues

In general, the team considered the identification of equipment deficiencies at

Susquehanna to be adequate. There was a low threshold for the identification of

individual issues, 23,000 ARs were written per year, and about 4,000 of those were

sub-classified as CRs. The housekeeping and cleanliness of the plant was generally

good; the general cleanliness of the plant enhanced the ability of personnel to more

easily identify equipment deficiencies and monitor equipment for worsening conditions.

Notwithstanding, during a tour of the facility, the inspectors observed that high density

concrete shield blocks were stacked on pallets in the vicinity of the Unit 1 recirculation

Enclosure

8

motor generator sets. The blocks were pre-staged for work during the upcoming

refueling outage, and were in a heavily trafficked area of the turbine building. There was

a painted warning on the floor, near the pallets, that the floor loading should not exceed

400 pounds per square foot (psf). When the inspectors asked whether the weight of the

blocks was within the rated floor load limit, it was determined that this condition had not

been identified and documented as acceptable. Initially, Susquehanna personnel

concluded that the blocks exceeded the posted limit and moved the pallets to reduce the

floor loading. Subsequently, Susquehanna weighed the pallets and blocks and

determined that they did not exceed the allowable floor loading. Based on this

evaluation the inspectors concluded the missed identification of this issue was minor.

The issue was documented in CR 954950.

The team also identified that several ARs were not classified as CRs, commensurate

with the safety significance, as required by their procedure (NDAP-QA-0702, Action

Request and Condition Report Process). The result was that the issues did not go to

the Screening Team, did not receive the necessary management attention, and were not

corrected in a timely manner (CR 957319). In addition, ARs are not normally trended to

allow the identification of an adverse change in performance. With the exception of the

first example, the below are considered procedure violations of minor significance due to

no impact on the related equipment. As such, these issues are not subject to

enforcement action, in accordance with the NRC=s Enforcement Policy.

Examples include:

C

AR/CPG/OPS 751412, initiated February 2, 2006, identified that the Low Pressure

Injection Permissive setpoint was not changed in the residual heat removal (RHR)

and core spray (CS) operating procedures. The setpoint was changed in 1999, as

part of a modification; the procedures were not changed until July 2007. (See

Section 4OA2.a.3(d) for additional details.)

C

AR/OPS/CSHIFT 777335, initiated July 25 2006, identified that an operator started

the suppression pool (SP) filter pump contrary to the procedure. The AR was closed

with no documented corrective actions taken.

The safety significance is that the operator did not operate the safety-related system

in accordance with the licensees written procedures and the Technical

Specifications (TS). The documentation of corrective actions should have included a

determination of the affects of starting of the pump, and counseling of the operator

on the requirement to follow procedures.

C

AR/CPG 810513, initiated September 16, 2006, identified that the wrong valve

numbers were listed for the emergency service water (ESW) system valves for the

E EDG. As of the inspection, the procedure had not been changed.

The safety significance is that operators may not have been able to use the

licensees written procedure to align the ESW system in support of the operation of

the swing E EDG in a timely manner.

Enclosure

9

C

AR/CPG/I&C 938054, initiated December 10, 2007, identified that a functional testing

and calibration procedure for the RHR service water radiation monitor could not be

performed, as written. As of the inspection, corrective actions had not been taken.

an inconsistency between the procedures and the design basis for SP cooling was a

CAQ, which resulted in corrective actions not being taken for two years to the time of the

inspection. Although the inconsistency was identified in 2006, Susquehanna personnel

did not recognize that the issue impacted current plant operations; as a result, the issue

was not scheduled for resolution in a timely manner. The team noted that, although

Susquehanna had classified the issue as a CR, it was considered to be NAQ - not a

CAQ - and was not scheduled for evaluation until the EPU had been approved. Refer to

Section 4OA2.a.3(b) for a detailed discussion of the finding.

(b)

Prioritization and Evaluation of Issues

The team determined that Susquehannas performance in this area was adequate.

Notwithstanding the above discussion of some ARs not being classified as CRs, the

station appropriately reviewed those CRs that went to the Screening team and properly

classified them for significance. The discussions about specific topics at the Screening

meetings were detailed, and there were no classifications or immediate operability

determinations with which the team disagreed. The team considered the contributions of

the CARB to add value to the CAP process. One CARB review was noted to be

particularly insightful with respect to the quality of the causal analysis for CR 773046.

The CR identified problems with the closing of CRs by the nuclear training department

without completing all the required actions. The team did not identify any items in the

operations, engineering, or maintenance backlogs that were risk significant, individually

or collectively. In addition, the quality of the causal analyses reviewed was generally of

adequate technical detail and scope to identify causal factors and develop effective

corrective actions. The team noted that the RCA for the NCV from the last PI&R

inspection related to scaffolding was effective in that there had not been significant

recurrences of inadequate scaffold installations since the evaluation was completed.

With regard to operability evaluations, the team observed that, an operability

determination for the PAM level instruments, conducted in response to an inconsistency

between the FSAR and EOPs, determined that the level instruments would be operable.

(The inconsistency between the FSAR and the EOPs is described in detail in section

4OA2.a.3(b).) During follow-up discussions, the inspectors were told by operations and

engineering personnel that all of the PAM instrumentation together functioned to provide

the needed indications to the operators, and that the RPV level indications were not

needed after the initial entry into the EOPs. This was not consistent with the

requirements for the operability of each individual function of the PAM, as detailed in TS 3.3.3.1. Although subsequent discussions with the Susquehanna staff determined that

the most (if not all) of the PAM RPV level instruments would indicate post-LOCA, the

initial operability determination and statements during the inspection did not consider

that the PAM level instruments are required to be operable post-accident regardless of

whether EOPs have been entered. This issue was related to the performance

Enclosure

10

deficiencies discussed in findings 4OA2.a.3(a), (b) and (c), and is not identified as an

additional finding. The issue was entered into the CAP as AR/CR964836.

(c)

Effectiveness of Corrective Actions

No findings of significance were identified in the area of effectiveness of corrective

actions. The team determined that the effectiveness of corrective actions at

Susquehanna was generally good. The control of scaffolds was a significant problem

during the last PI&R inspection; the team noted that oversight of scaffolds has improved,

but station personnel continue to identify examples where the scaffold does not appear

to be built in accordance with the procedure. In addition, the team identified

weaknesses in the scaffold procedure, such as allowing the installer to approve

deviations from the approved construction. During the inspection, the procedure was

revised, and plans were developed for engineering to review all current deviations.

3.

Findings

(a)

Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG Resulted in an

Inadequate Procedure

Introduction: The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, because Susquehanna failed to adequately

evaluate a deviation from the Boiling Water Reactor Owners Group Emergency

Procedure Guidelines / Severe Accident Guidelines (BWROG EPG/SAG), which

resulted in one of the Emergency Operating Procedures (EOPs) being inadequate.

Description: On January 5, 2006, AR/CR 739371 was initiated to document an

inconsistency between the EOPs and assumptions in the Final Safety Analysis Report

(FSAR) regarding the initiation of suppression pool cooling. Specifically, it was identified

that the assumptions used in evaluating SP temperature response for the most limiting

design basis accident (DBA) loss of coolant accident (LOCA) did not appear to be

consistent with direction provided in the EOPs.

During this inspection, the team noted that the Susquehanna EOPs were not consistent

with the BWROG EPG/SAG. Specifically, BWROG EPG/SAG, Revision 2, Caution #1,

warned the operators that reactor pressure vessel (RPV) level instrumentation may be

unreliable if the temperatures near the instrument sensing lines exceeded RPV

saturation temperature. The EPG Bases stated that the purpose of Caution #1 was to

give the operators a chance to evaluate the validity of the RPV level instrumentation, in

order to avoid premature entry into the RPV flooding contingency procedure before it

was appropriate to do so. Susquehanna did not adequately evaluate the deviation from

the generic guidance in the EPG/SAG with respect to the caution. The Susquehanna

EOPs did not use a Caution statement, which would have allowed the operators the

opportunity to evaluate the level instrumentation; but instead, changed the caution to a

procedural step which directed the operators to transition directly to the RPV Flooding

procedure. Specifically, EO-100-103-1, Primary Containment Cooling, step DWT-3,

Enclosure

11

directed the operators to transition to contingency procedure EO-000-114-1, RPV

Flooding, when drywell temperature exceeded RPV saturation temperature.

The evaluation for the deviation was not completed in accordance with the requirements

of procedure NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and

Writers Guide. The procedure required that all deviations be evaluated to determine if

the deviation was technically justified and appropriate. Susquehanna documented that

the deviation was a minor difference from the generic guidelines in 50.59 Safety

Evaluation NL-92-019 (October 29, 1998) and 50.59 Screen 5059-01-976 (July 3, 2002).

The evaluation was based on an overly conservative assumption that all RPV level

instrumentation would be lost after a DBA LOCA. The reviews did not evaluate the

potential adverse consequences associated with the deviation, including the potential

impact on the SP cooling safety function. Immediate corrective actions included the

initiation of an informational Night Order to the control room operators explaining the

issue, and the cessation of all simulator scenarios that involve the use of EO-100-103-1

until the issue is resolved.

The performance deficiency is the failure to adequately evaluate a deviation from the

BWROG EPG/SAG, which resulted in one of the EOPs being inadequate for use by the

operators in the event of a DBA LOCA. Specifically, under some accident conditions,

the EOPs would have unnecessarily directed entry into RPV flooding which would have

limited the availability of SP cooling and complicated the operators response to the

event.

Analyses: This performance deficiency is more than minor because it is associated with

the Procedure Quality (EOP) attribute of the Mitigating Systems cornerstone and affects

the objective to ensure the availability, reliability, and capability of systems that respond

to initiating events to prevent undesirable consequences. Specifically, the EOP could

have directed entry into the RPV flooding procedure unnecessarily which would have

restricted the use of suppression pool cooling and required other actions that would have

complicated the operators response to the event. The inspectors performed a review of

the finding in accordance with NRC Inspection Manual Chapter (IMC) 0609,

Significance Determination Process (SDP), Attachment 4, Phase 1 - Initial Screening

and Characterization of Findings, and determined that the finding screened out as

having very low safety significance (Green), because it was not a design deficiency, did

not result in an actual loss of safety function, and did not screen as potentially risk

significant due to external initiating events.

Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, states, in part, that activities affecting quality shall be prescribed by

documented procedures appropriate to the circumstances and that the activities shall be

accomplished in accordance with the procedures. Contrary to the above, Emergency

Operating Procedure EO-100-103-1, Primary Containment Cooling, was inadequate, in

that it directed the operators to transition directly to the RPV Flooding procedure when

RPV level instruments may have been available, which resulted in limiting the availability

of SP cooling. However, because the finding was of very low safety significance (Green)

Enclosure

12

and has been entered into the CAP (AR/CR 962881), this violation is being treated as an

NCV, consistent with section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000387/2008006-01; 05000388/2008006-01 - Failure to Adequately Evaluate

a Deviation from BWROG EPG/SAG Resulted in an Inadequate EOP)

(b)

Failure to Identify and Correct Inconsistencies Between the FSAR and the EOPs

Introduction: The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, for the failure to identify that an inconsistency between the

emergency operating procedures and the design basis for SP cooling was a CAQ, which

resulted in corrective actions not being taken for two years to the time of the inspection.

Although the inconsistency was identified in 2006, Susquehanna personnel did not

recognize that the issue impacted current plant operations; as a result, the issue was not

scheduled for resolution in a timely manner. The assumption in the FSAR for the DBA

LOCA stated that SP cooling would be implemented ten minutes after entry into the

EOPs. The EOPs would not have allowed initiation of SP cooling for an extended period

of time.

Description: On January 5, 2006, AR/CR 739371 was initiated to document an

inconsistency between the EOPs and design basis assumptions for the SP cooling

response. The problem was identified during Susquehannas review in support of the

extended power uprate (EPU) project. Specifically, Susquehanna Engineering identified

that the assumptions used in evaluating SP temperature response for the most limiting

LOCA did not appear to be consistent with direction provided in the EOPs. The team

noted that, although Susquehanna personnel had classified the issue as a CR, they did

not recognize that the issue impacted current plant operations. Therefore, it was

considered to be NAQ - not a condition adverse to quality - and was not scheduled for

evaluation until the EPU had been approved.

The Susquehanna FSAR, Section 6.2.1.1.3, stated that the maximum SP temperature

would result from a reactor recirculation suction line break. The drywell pressure and

temperature response analyses assumed that RHR heat exchangers were activated

about ten minutes after entry into the EOPs to remove energy from the drywell by

cooling the SP. The CR identified that, in the event of a DBA LOCA, the EOPs would

direct operators to implement the RPV flooding procedure (EO-000-114) to maintain

adequate core cooling, and this required that all available RHR flow be used to flood the

RPV up to the steam lines. The initiators concern was that this would delay establishing

flow through a RHR heat exchanger for SP cooling, because of the unique design of the

RHR system at Susquehanna, and therefore would be inconsistent with the accident

analyses assumptions. In addition, the CR stated that it was assumed in the EOPs that

all RPV water level indications would be unreliable and therefore unavailable for this

scenario. Susquehanna personnel informed the team that they had not evaluated the

issues documented in the CR, at the time it was initiated, because they had assumed

that they were only associated with EPU and not current plant operation. Immediate

corrective actions included the start of an evaluation during the inspection of the

identified inconsistency for SP cooling, and additional guidance to the operators.

Enclosure

13

The performance deficiency is the failure to properly categorize the inconsistency

between the FSAR and the EOPs as a CAQ, which resulted in the deficiency not being

corrected in a timely manner commensurate with its safety significance.

Analyses: The performance deficiency is more than minor because it is associated with

the Design Control attribute of the Mitigating Systems cornerstone and affects the

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, in the event of a

DBA LOCA, SP cooling would not be initiated within the time frame assumed in the

FSAR, which could affect the capability of the system to perform its safety function

consistent with the design basis. The inspectors performed a review of the finding in

accordance with IMC 0609, and determined that the finding screened out as having very

low safety significance (Green) because it was not a design deficiency, did not result in

an actual loss of safety function, and did not screen as potentially risk significant due to

external initiating events.

This performance deficiency has a cross-cutting aspect in the area of Problem

Identification and Resolution (PI&R), Corrective Action Program (CAP), because

Susquehanna did not identify that the inconsistency documented in the CR should have

been categorized as a CAQ, commensurate with its safety significance. P.1(a)

Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, states, in part,

that conditions adverse to quality shall be promptly identified and corrected. Contrary to

the above, Susquehanna failed to identify that the nonconformance identified in AR/CR

739371, January 2006, was a CAQ; this resulted in the condition not being corrected for

over two years. However, because the finding was of very low safety significance

(Green) and has been entered into the corrective action program (AR/CR 959670), this

violation is being treated as an NCV, consistent with section VI.A.1 of the NRC

Enforcement Policy.

(NCV 05000387/2008006-02; 05000388/2008006-02 - Failure to Identify and Correct

Inconsistencies Between the FSAR and the EOPs)

(c)

Failure to Accurately Model the Simulator for RPV Water Level Instrumentation

Introduction: The NRC identified a Green NCV of 10 CFR 55.46(c)(1), Plant

Referenced Simulators, because the Susquehanna plant-referenced simulator did not

accurately model RPV level instrument response following a DBA LOCA. Specifically,

the RPV level instruments in the simulator were programmed to fail high after a LOCA,

and the expected plant response is that the instruments should indicate properly.

Description: As part of the teams follow-up on the issues in AR/CR 739371, the

inspectors questioned the concern stated in the CR, that the operators would need to

enter the RPV flooding procedure during a DBA LOCA due to a loss of valid RPV level

instrumentation. The inspectors reviewed the Susquehanna specific EOPs and

supporting documents, and determined that the Susquehanna EOP Plant Specific

Enclosure

14

Technical Guideline (PSTG) description of the expected response of the RPV level

instrument response to LOCA events, was based on analysis, EC-SIMU-1001,

Evaluation of Simulator Level Instrument Response to Large LOCA, dated May 4,

1994. The analysis was performed to determine if the observed simulator response

during a large break LOCA (RPV level instrumentation off-scale high) was consistent

with the expected plant response. The analysis assumed that the drywell would

experience superheated conditions, which would cause RPV water level instrumentation

reference leg flashing and a subsequent loss of all RPV level indication. The analysis

concluded that the simulator response reasonably predicted the expected actual plant

response during a large break LOCA event. The expected plant response, as stated in

the analysis, was incorrect; in that a LOCA would not always cause a loss of all RPV

level instruments.

On January 29, 2008, the inspectors observed two scenarios in the simulator to evaluate

the response to a DBA LOCA, with all safety systems available. The inspectors

observed that the RPV level instruments did indicate off-scale high shortly after the

initiation of the event, consistent with the analysis. The inspectors questioned the basis

of the analysis; specifically, why Susquehanna believed that the level instruments would

not be available after a DBA LOCA event. Subsequently, Susquehanna determined that

the RPV level instrument reference legs were not expected to routinely flash during a

DBA LOCA, and that the analysis had been based on an overly conservative assumption

that the drywell would always reach superheated conditions post-LOCA. Immediate

corrective actions included the initiation of an informational Night Order to the control

room operators explaining the issue, and the cessation of all simulator scenarios that

involve the use of EO-100-103-1 until the issue is resolved.

The performance deficiency is that Susquehanna did not ensure that the plant

referenced simulator accurately modeled the expected plant response for RPV level

instrumentation after a DBA LOCA, resulting in negative training of the licensed

operators.

Analyses: This performance deficiency is more than minor because it is associated with

the Human Performance attribute of the Mitigating Systems cornerstone and affects the

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the incorrect

modeling of the Susquehanna plant referenced simulator introduces negative operator

training that could affect the ability of the operators (a mitigating system) to take the

appropriate actions during an actual event. The simulator training conditioned the

operators to expect the level instruments to be unavailable during events that cause

drywell temperatures to reach or exceed RPV saturation temperature. As a result,

during an actual event, the operators could prematurely transition into the RPV flooding

procedure when the RPV level instruments should be providing valid indication. The

inspectors evaluated the finding in accordance with IMC 0609, Appendix I, Licensed

Operator Requalification Significance Determination Process. The finding was

determined to be of very low safety significance (Green) because it is not related to

operator performance during requalification, it is related to simulator fidelity, and could

have a negative impact on operator actions.

Enclosure

15

Enforcement: 10 CFR 55.46(c)(1), Plant Referenced Simulators, states, in part, that a

plant referenced simulator must demonstrate expected plant response to normal,

transient, and accident conditions. Contrary to the above, as of January 2008, the

Susquehanna plant referenced simulator did not accurately demonstrate the actual

expected plant response of the RPV water level instrumentation following a DBA LOCA,

which could result in negative operator training. However, because the finding was of

very low safety significance (Green) and has been entered into the CAP (AR/CR

962881), this violation is being treated as an NCV, consistent with section VI.A.1 of the

NRC Enforcement Policy.

(NCV 05000387/2008006-03; 05000388/2008006-03 - Failure to Accurately Model

the Simulator for RPV Water Level Instrumentation)

(d)

Failure to Identify and Correct a Setpoint Error in the RHR and CS Operating

Procedures

Introduction: The NRC identified a Green NCV of 10 CFR 50, Appendix B, Criterion XVI,

Corrective Action, for the failure to identify that a setpoint error in the operating

procedures for safety-related systems was a CAQ, resulting in the procedures not being

corrected in a timely manner. Specifically, in February 2006, Susquehanna personnel

identified an incorrect setpoint for the low pressure injection permissive interlock in the

RHR and CS systems operating procedures and associated hard cards; however, the

procedures were not revised until July 2007 due to the issue being screened as low

priority and not a condition adverse to quality (CAQ).

Description: On February 11, 2006, an AR was written to identify that the low pressure

injection permissive setpoint in the RHR and CS operating procedures, and the

associated operator hard cards, was incorrect. The correct setpoint is 420 pounds per

square inch gage (psig), but the procedures still had the previous setpoint of 436 psig.

The setpoint had been changed in 1999 as part of a modification. The procedures were

not revised until July 16, 2007, 17 months after the deficiency was identified in an AR. In

addition, the inspectors noted that the setpoint in the procedures (436 psig) was not

within the allowable tolerance (407-433 psig) listed in the Susquehanna TS, Section 3.3.5.1, Emergency Core Cooling System (ECCS) Instrumentation.

When the AR was initiated, it was sub-classified as AR/CPG/OPS; that is, assigned to

the Central Procedures Group and identified as an Operations procedure. It was not

recognized that deficient operating procedures for safety-related systems may be a CAQ

and that the AR should have been classified as a Condition Report. The affected

section in the procedures was the verification of the response of the systems to an

automatic initiation signal. For example, the Unit 1 RHR procedure OP-149-001, RHR

System, Section 2.2, noted that No operator action is required unless an automatic

action failed to occur ... At 436 psig decreasing Reactor pressure, RHR INJ OB ISO

[injection outboard isolation] HV-151-F015A & B OPEN. If the valves did not open at

the specified pressure in the procedure and hard card, the operator may have diverted

their attention unnecessarily and attempted to open the valve manually, even though the

Enclosure

16

interlock would not have been satisfied (420 psig) and the valve would not open in

accordance with the plant design.

The pressure switches were changed in 1999, as part of a Unit 1 plant modification

(Design Change Package (DCP) 97-9075); Unit 2 switches were changed by DCP

97-9076. The modification replaced the existing pressure switches with Barton pressure

indicating switches, because of improved accuracy. The low pressure injection

permissive interlock prevents the CS and RHR injection valves from opening until

reactor pressure has decreased to the RHR and CS systems design pressure, to

prevent over pressurization of the RHR and CS systems. The DCP identified the

specific RHR and CS operating procedures as needing to be changed. Immediate

corrective actions included the initiation of a new CR to evaluate the other pending

procedure changes to determine if their priority should be revised.

The performance deficiency involved a failure to identify and correct a CAQ, the

incorrect setpoint, in a timely manner commensurate with its safety significance. The

inspectors concluded this action was untimely because the modification process would

have revised these procedures prior to the modification being accepted by operations

personnel.

Analysis: The performance deficiency is more than minor because it is associated with

the Procedure Quality attribute of the Mitigating Systems cornerstone and affects the

objective to ensure the availability, reliability, and capability of systems that respond to

initiating events to prevent undesirable consequences. Specifically, the incorrect

setpoint reference in the procedure impacted the reliability of operator response to the

event in that it could delay operator actions or result in misoperation of equipment. The

inspectors performed a review of the finding in accordance with NRC Inspection Manual

Chapter (IMC) 0609, Significance Determination Process (SDP), Attachment 4, Phase

1 - Initial Screening and Characterization of Findings. The inspectors determined that

the finding screened out as having very low safety significance (Green), because it was

not a design deficiency, did not result in an actual loss of safety function, and did not

screen as potentially risk significant due to external initiating events

This performance deficiency has a Cross-Cutting aspect in the area of PI&R, CAP,

because Susquehanna did not identify that a setpoint error in operating procedures for

safety-related systems was a CAQ, commensurate with its safety significance. P.1(a)

Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, states, in part,

that conditions adverse to quality shall be promptly identified and corrected. Contrary to

the above, from 1999, when the pressure switches were replaced and the setpoint was

changed, until 2006, when AR 751412751412was written, Susquehanna had failed to identify

that the setpoint was wrong for the low pressure injection permissive interlock in the

operating procedures for RHR and CS. Subsequently, on February 11, 2006, when

Susquehanna personnel initiated and approved AR 751412751412 they failed to identify that

the stated deficiency was a CAQ, which resulted in untimely corrective actions.

Susquehanna considered this to be a procedure change and not a CAQ, and classified

the AR as a CPG versus a CR. As such, the procedures were not changed until July 16,

Enclosure

17

2007, 17 months after the condition was identified and eight years after the setpoint was

changed in the plant. Because this finding is of very low safety significance (Green), and

was entered into the Susquehanna CAP (AR/CR 956917) this violation is being treated

as a Non-Cited Violation (NCV) consistent with Section VI.A.1 of the NRC Enforcement

Policy.

(NCV 05000387/2008006-04; 05000388/2008006-04 - Failure to Identify and Correct

a Setpoint Error in the RHR and CS Operating Procedures)

b.

Assessment of the Use of Operating Experience

1.

Inspection Scope

The team reviewed a sample of operating experience (OE) issues for applicability to

Susquehanna, and for the associated actions. The documents were reviewed to ensure

that underlying problems associated with the issues were appropriately considered for

resolution. The team also reviewed how Susquehanna considered OE for applicability in

causal evaluations.

Prior to the start of the inspection, the inspectors noted a potential negative trend in the

number of issues associated with reactivity management. In accordance with the

Inspection Procedure, the inspectors increased the scope of the review to determine if

there was an adverse trend in the area of reactivity management over the past five

years. The inspectors reviewed select ARs and CRs associated with the control rod

drive system, control rod problems, human performance issues, and the spent fuel pool;

the inspectors review included how Susquehanna had incorporated applicable OE for

these specific systems and human performance issues into the CAP. The inspectors

interviewed selected licensee staff.

2.

Assessment

In general, OE was effectively used at the station. The inspectors noted that OE was

reviewed during the causal evaluation process and incorporated, as appropriate, into the

development of the associated corrective actions. The inspectors noted that OE was

frequently used in work packages and pre-job briefs. The team did not identify any

significant deficiencies within the sample reviewed. The team did not identify a negative

trend nor any significant problems with the control of activities associated with reactivity

management.

3.

Findings

No findings of significance were identified in the area of operating experience.

c.

Assessment of Self-Assessments and Audits

1.

Inspection Scope

Enclosure

18

The team reviewed a sample of departmental self-assessments, CAP trend reports, and

Quality Assurance (QA) audits, including QAs most recent audit of the CAP. The team

also reviewed the latest internal assessment of the safety culture at Susquehanna,

conducted in October 2006. The reviews were performed to determine if problems

identified through these evaluations were entered into the CAP system, and whether the

corrective actions were properly completed to resolve the deficiencies. The

effectiveness of the audits and self-assessments was evaluated by comparing audit and

self-assessment results against self-revealing and NRC-identified findings, and

observations during the inspection.

2.

Assessment

The team considered the quality of the audits and self-assessments to be thorough and

critical. ARs were initiated for issues identified by QA and the self-assessments. The

Susquehanna 2006 Comprehensive Cultural Assessment Report consisted of a safety

culture survey and interviews. The cultural assessment report identified some

weaknesses at the station, which were entered into the CAP. The team did not identify

any results that were inconsistent with Susquehannas conclusions.

3.

Findings

No findings of significance were identified in the area of audits and self-assessments.

d.

Assessment of Safety Conscious Work Environment

1.

Inspection Scope

To evaluate the safety conscious work environment (SCWE) at Susquehanna, during

interviews and discussions with station personnel, the team assessed the workers

willingness to enter issues into the CAP and to raise safety issues to their management

and/or to the NRC. The inspectors also interviewed the Employee Concerns Program

(ECP) representative to determine if employees were aware of the program and had

used it to raise concerns. The team reviewed a sample of the ECP files to ensure that

issues were entered into the corrective action program, as appropriate.

2.

Assessment

Based on interviews, observations of plant activities, and reviews of the ARs and ECP,

the inspectors determined that the site personnel were willing to raise safety issues and

document them in ARs. Individuals actively utilized the AR system, as evidenced by the

number and significance of issues entered into the program. The inspectors noted that

ARs were written by a variety of personnel, from workers to managers. ECP evaluations

were thorough and appropriate actions were taken to address issues.

3.

Findings

No findings of significance were identified related to the SCWE at Susquehanna.

Enclosure

19

4OA6 Meetings, Including Exit:

On February 1, 2008, the team presented the inspection results to Mr. B. McKinney,

Senior Vice President, and to other members of the Susquehanna staff, who

acknowledged the findings. The team confirmed that no proprietary information

reviewed during the inspection was retained.

ATTACHMENT: Supplemental Information

In addition to the documentation that the team reviewed (listed in the Attachment),

copies of information requests given to the licensee are in ADAMS, under accession

number ML080430585.

Attachment

A-1

ATTACHMENT - SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel:

M. Adelizzi, Risk Engineer

N. DAngelo, Manager, Station Engineering

C. Gannon, Vice President, Nuclear Operations

T. Gorman, Project Manager, Design Engineering

R. Hoffman, Manager, Nuclear Fuels & Analysis

B. McKinney, Chief Nuclear Officer

I. Missien, Project Manager, System Engineering

B. ORourke, Senior Engineer, Nuclear Regulatory Affairs

R. Pagodin, General Manager, Nuclear Engineering

R. Paley, General Manager, Plant Support

A. Price, Supervisor, Corrective Action & Assessment

M. Rochester, Employee Concerns Representative

G. Ruppert, Manager, Maintenance

R. Schechterly, Operating Experience Coordinator

R. Sgarro, Manager, Nuclear Regulatory Affairs

M. Sleigh, Security Manager

B. Stitt, Operations Training

T. Tonkinson, Supervisor, Maintenance Support

D. Weller, Maintenance Foreman

L. West, Supervisor, Central Procedure Group

Nuclear Regulatory Commission:

M. Gray, Branch Chief, Technical Support & Assessment

F. Jaxheimer, Senior Resident Inspector

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed: 05000387/2008006-01

05000388/2008006-01

NCV Failure to Adequately Evaluate a Deviation from BWROG EPG/SAG

Resulted in an Inadequate EOP

(Section 4OA2.a.3 (a))05000387/2008006-02

05000388/2008006-02

NCV Failure to Identify and Correct Inconsistencies in the Licensing Basis

and the EOPs

(Section 4OA2.a.3 (b))05000387/2008006-03

05000388/2008006-03

NCV Failure to Accurately Model the Simulator for RPV Water Level

Instrumentation

(Section 4OA2.a.3 (c))05000387/2008006-04

05000388/2008006-04

NCV Failure to Identify and Correct a Setpoint Error in the RHR and CS

Operating Procedures

(Section 4OA2.a.3 (d))

Attachment

A-2

LIST OF DOCUMENTS REVIEWED

Procedures:

BWROG EGP/SAG and Appendix B Bases, Revision 2

Design Considerations Applicability Sheet Number 42, Emergency Plan, Revision 1

EO-000-102, RPV Control, Revision 2

EO-000-114-1, RPV Flooding, Revision 5

EO-100-103-1, Primary Containment Control, Revision 9

EP-AD-014, Surveillance Testing of Emergency Communications Equipment, Revision 10

EP-AD-015, Review, Revision, and distribution of the SSES Emergency Plan, Revision 11

ME-0RF-161, Control of Fuel Pool Cleanout Activities, Revision 5

ME-0RF-163, Fuel Pool Cleanout - Energy Solutions - Dose Rate Profiling of Irradiated

Hardware and Liners, Revision 4

MFP-QA-1220, Engineering Change Process Handbook, Revision 2

MI-VL-009, Operation of Leak Rate Monitors, Surge Tank Assemblies and 1035 psig Test

Pumps, Revision 3

MT-AD-504, Scaffold Erection, Review and Inspection, Revisions 9 & 10

MT-GM-018, Freeze Sealing of Piping, Revision 15

MT-GM-050, Limitorque Type SMB-000 through SMB-4 Operator Maintenance, Revision 12

NASP-QA-202, Independent Technical Review Program, Revision 2

NASP-QA-401, Internal Audits, Revision 9

NASP-QA-700, Performance Assessment Process, Revision 0

NDAP-00-0109, Employee Concerns Program, Revision 10

NDAP-00-0708, Corrective Action Review Board, Revision 4

NDAP-00-0710, Station Trending Program, Revision 1

NDAP-00-0745, Self-Assessment, Benchmarking and Performance Indicators, Revision 7

NDAP-00-0751, Significant Operating Experience Report (SOER) Review Program, Revision 3

NDAP-00-0752, Cause Analysis, Revisions 3 and 4

NDAP-00-0753, Common Issue Analysis, Revision 0

NDAP-00-0778, Performance Improvement Program, Revision 2

NDAP-QA-0103, Audit Program, Revision 9

NDAP-QA-0330, PSTG and Emergency Procedures, Revision 8

NDAP-QA-0330, Symptom Oriented EOP and EP-DS Program and Writers Guide, Revision 3

NDAP-QA-0412, Leakage Rate Test Program, Revision 10

NDAP-QA-0702, Action Request and Condition Report Process, Revision 20

NDAP-QA-0703, Operability Assessments and Requests for Enforcement Discretion,

Revision 12

NDAP-QA-0720, Station Report Matrix and Reportability Evaluation Guidance, Revision 13

NDAP-QA-0725, Operating Experience Review Program, Revision 11

NDAP-QA-0726, 10CFR50.59 and 10CFR72.48 Implementation, Revision 10

NDAP-QA-1220, Engineering Change Process, Revision 2

NTP-QA-53.1, Susquehanna Fire Brigade Training Program, Revision 15

ODCM-QA-001, ODCM Introduction, Revision 3

ODCM-QA-002, ODCM Review and Revision Control, Revision 4

ODCM-QA-003, Effluent Monitor Setpoints, Revision 3

ODCM-QA-004, Airborne Effluent Dose Calculations, Revision 4

ODCM-QA-005, Waterborne Effluent Dose Calculation, Revision 3

Attachment

A-3

ODCM-QA-006, Total Dose Calculation, Revision 2

ODCM-QA-007, Radioactive Waste Treatment Systems, Revision 2

ODCM-QA-008, Radiological Environmental Monitoring Program, Revision 11

ODCM-QA-009, Dose Assessment Policy Statements, Revision 2

ON-145-004, RPV Water Level Anomaly, Revision 13

OP-024-001, Diesel Generators, Revision 49

OP-024-004, Transfer and Test Mode Operations of Diesel Generator E, Revision 26

OP-149-001, RHR System, Revisions 31 and 32

OP-151-001, Core Spray System, Revisions 27 & 28

SE-124-007, Unit 1 Division 1 Diesel Generator LOCA LOOP Test, Revision 15

SE-259-044, LLRT of RHR Containment Spray Penetration Number X-39A, Revision 11

SOP-054-B03, Quarterly ESW Flow Verification Loop B, Revision 7

SSES-EPG, SSES Plant Specific Technical Guideline, Revision 9

Audits:

666178, Corrective Action, November 2006 - February 2007

667966, QA Internal Audit Report, Fuel Management, Revision 0

691277, QA Internal Audit Report Access Authorization and Fitness for Duty, Revision 0

706249, Operations Training and Qualification Programs, May - June 2007

718607, QA Internal Audit Report, Engineering, Revision 0

744333, Operations, November - December 2007

792034, QA Internal Audit Report, Security, Revision 0

NEIP Audit of Susquehanna Quality Assurance, June 2006

Self-Assessments:

2006 Comprehensive Cultural Assessment, September - October 2006

CA&A Functional Unit Excellence Plan, 1st, 2nd, and 3rd Quarters 2007

CAA-06-01, Site Wide Self-Assessment, December 2006

CAA-06-05, Self-Assessment Program Performance, February 2006

CAA-06-08, Decrease in CR Generation Identified by Trend Report, November 2006

Focused Self Assessment, MOV Program Self-Assessment, October 2007

Maintenance Implementing Procedures Adequacy for Qualified, Inexperienced Employees,

June 2007

Multi-Utility Joint Audit Program Initiative, March - April 2007

NTG Focused Self-Assessment of Operator Training Programs, June 2007

OPS-06-02, Determine the Status of Operator Fundamentals, February 2006

OPS-06-03, Operations Focused Se-f Assessment, July 2006

Pre-PI&R Focused Self-Assessment, September 2007

QA Organization Effectiveness Self-Assessment, October 2006

QA-06-01, Operations QA Audit Preparation Gap Analysis for QC, May - July 2006

SEC-06-01, Analyses of SSES Security Procedures and Physical Security Plan, Revision 0

Attachment

A-4

Action Requests (* denotes an AR/CR generated as a result of this inspection):

478369

524893

542157

545804

549328

554362

554598

555140

555263

555562

557348

565795

575128

578943

584400

591033

594366

594887

595165

604009

604296

610978

615707

623914

623949

635924

647827

655735

666405

668871

669732

677145

687080

688300

691108

693936

699781

723483

723976

724102

724165

724374

724467

724717

726672

728295

728936

730852

730944

730947

737236

738555

738575

738634

738653

738907

738999

739262

739371

739371

739386

739419

739579

739625

739713

739737

740043

740073

740303

740477

740538

740658

740668

740723

740802

740804

740825

740946

740948

740955

740988

741041

741321

741457

741707

741908

741943

742191

742318

742342

742427

742676

742966

743043

744975

744979

745221

745248

745462

745773

746658

747077

747438

749294

749341

749832

750140

750232

751212

751412

751433

751444

752341

752347

752582

753392

753664

753869

753990

755360

756094

756415

756804

757530

757979

758337

759209

759216

759827

760281

760526

760526

762497

763050

763128

763397

764145

764738

764953

765421

767566

767567

768301

768502

768821

768920

769304

769867

769870

770453

771319

771876

771961

773046

773409

774453

774475

774509

774549

775285

775718

776112

776171

776769

776918

777335

777723

778124

779830

780144

780155

780778

780992

781644

782321

782344

783655

784730

784882

784890

785561

785791

786149

786224

786564

786735

786768

787850

788616

788621

788879

789971

791115

791329

792158

793381

794995

795583

796640

797517

799890

802254

802539

802563

802572

802697

805698

806710

809503

809702

810391

810513

811239

811429

811996

812948

813844

815268

816097

816710

817720

818082

818154

820344

820380

820989

820995

821006

821064

822996

823908

824522

824895

825107

825750

826452

826870

827023

827966

828626

828744

829065

829502

835002

837153

837180

839753

841169

841885

842663

842920

843144

843985

845441

849935

851918

853358

854681

855266

855268

856997

858269

858578

859082

859440

859794

859839

860299

860551

861162

861366

861415

862474

864090

865286

865423

865804

865924

866930

867534

867747

867881

868251

868259

868828

868874

869819

869824

870968

871013

872039

872056

873026

873683

873741

873919

874227

875597

875976

876021

876427

877419

877727

877743

878165

878326

879080

879847

880331

880573

880702

880806

881210

881219

881225

881236

882318

883987

886209

887048

887067

888310

889683

889966

891288

891733

891795

892142

892152

892528

893090

893157

893290

895147

896455

896505

896685

897250

898909

899429

900301

900720

901262

903439

904689

908163

911601

912213

912476

915167

915620

916453

916463

916873

917196

918392

918549

919470

927046

928515

929461

930075

930571

931113

932590

936060

936250

936370

936631

937123

938054

938698

938722

939516

939780

941290

941401

941626

941677

941810

947160

954950*

954970*

954972*

954975*

954990*

955072*

955073*

955111*

955130*

955150*

955151*

955761*

955780*

956339*

956344*

956431*

956696*

956914*

956917*

957319*

957484*

957637*

958769*

959670*

961655

962390

962881*

963061*

963065*

963698*

963861*

964512*

964514*

964836*

965167*

Attachment

A-5

Maintenance Work Requests (SPWO):

099065

099115

099120

099259

099364

448229

473889

570758

766396

766401

766406

766411

766413

766416

766496

767283

767284

767490

767506

767532

768234

768618

818282

862503

862569

862578

866262

866284

Non-Cited Violations and Findings Reviewed:

NCV 2005005-01, Inadequate FME Exclusion Procedural Instructions Associated with EDG

Work

FIN 2005009-01, Fire Brigade Drill Program Not Consistent with Regulatory Guidance and

Industry Standards

NCV 2006002-01, Equipment Hatch Plugs are Not Watertight as Indicated in FSAR

FIN 2006002-02, Incomplete Corrective Actions Contribute to CRD Flow Control Failure

NCV 2006003-01, Inadequate Procedures Resulted in Motor Operated Valve Failures

NCV 2006003-02, Failure to Identify Material Degradation which Resulted in the Failure of the

C ESW Pump Breaker

NCV 2006003-03, Inadequate Procedure Results in Elevated Reactor Coolant System Leakage

NCV 2006003-04, Inadequate Design Review of PRDNMS Modification Resulted in a Reactor

Scram

NCV 2006003-05, Ineffective Corrective Actions to Assure Training and Qualification of Workers

as Required by 10CFR50, Appendix B, Criterion XVI

NCV 2006004-01, Inadequate Risk Assessment

NCV 2006005-01, Inadequate Work Instructions for the Disassembly and Inspection of Check

Valves

NCV 2006005-02, Inadequate Evaluation of EPA Breaker Failures

NCV 2006006-01, Failure to Identify Scaffolding that Affected the Safety-Related RHR

Discharge Pressure Instrument Tubing Input to ADS

NCV 2006009-01, Safeguards Information

Licensee Identified NCV 2007002, U2 Div II Core Spray Pump Room (a High Radiation Area)

Was Not Posted and Was Open

Licensee Identified NCV 2007002, U1 HPCI Failed a Surveillance Due to the Failure to Perform

Preventive Maintenance

NCV 2007003-01, Failure to Take Timely Corrective Actions for an E EDG Jacket Water Leak

FIN 2007003-02, Failure to Maintain Occupational Radiation Exposure ALARA during Reactor

Water Cleanup Pipe Replacement Activities

FIN 2007003-03, Failure to Maintain Occupational Radiation Exposure ALARA during Outage

ISI of Reactor Pressure Vessel

NCV 2007003-04, Violation of 10CFR71.5 for Inadequately Secured Transport of Condensate

Pump Motors

NCV 2007003-05, Violation of 10CFR71.5 for Inadequately Accounting for Activity in a

Shipment of Irradiated Fuel Channels

Licensee Identified NCV 2007003, U2 Reactor Building HRA Postings and Boundary Moved

without Permission of RP

NCV 2007007-01, Inoperable ESSW Pump-House Ventilation Lineup

NCV 2007007-02, Failure to Use E EDG Procedure

Attachment

A-6

Miscellaneous:

5059-01-2356, 50.59 Screen of Specification C-1056, Long Term Scaffolding, Revision 4

CP067, Corrective Action Program - Evaluation & Resolution, Revision 8

(Lesson Plan & Student Material)

CP068, Managing the Corrective Action Process, Revision 2 (Lesson Plan & Student Material)

Daily CR Screening Team Package

Design Verification Checklist for SCN 6 for Specification C-1056, dated April 27, 2001

EC-059-1024, Design Requirements for and Evaluation of Potential Secondary Containment

Bypass Leakage Pathways, Revision 4

EC-RADN-1029, SSES Design Basis LOCA Dose Consequence Evaluation for Containment

Bypass Leakage Including the Effects of Suppression Pool Scrubbing, Revision 1

EC-SIMU-1001, Evaluation of Simulator Level Instrument Response to Large LOCA, dated

May 4, 1994

Engineering Specification C-1056, Erection of Scaffolding in Safety-Related Areas, Revision 4

EWR #MIS-85-0460, Design Inputs and Considerations Checklist for Specification C-1056,

Revision 2

Hot Box Item 08-01, Reactor Water Instrumentation Response during DBA LOCA, dated

January 31, 2008

IEEE Standard 497-2002, IEEE Standard Criteria for Accident Monitoring Instrumentation, dated

September 30, 2002

Long Term Scaffold Log, dated January 16, 2008

No Degraded Condition Response to OFR 963310, dated January 30, 2008

NRC Information Notice 2007-29, Temporary Scaffolding Affects Operability of Safety-Related

Equipment, dated September 17, 2007

NRC Inspection Procedure 42001, Emergency Operating Procedures, dated June 28, 1991

NRC Regulatory Guide 1.97, Instrumentation for Light-Water-Cooled Nuclear Power Plants to

Assess Plant and Environs Conditions During and Following an Accident, Revision 2

NRC Regulatory Issue Summary 2005-20, Information to Licensees Regarding Two NRC

Inspection Manual Sections on Resolution of Degraded and Nonconforming Conditions and

on Operability

NRC Regulatory Issue Summary 2007-21, Adherence to Licensed Power Limits, dated

August 23, 2007

NEDE-24801, Review of BWR Reactor Vessel Water Level Measurement, April 1980

NEDO-24708A, Additional Information Required for NRC Staff Generic Report on Boiling Water

Reactors, Revision 1

Operational Policy Statement (OPS) - 5, Deficiency Control System, Revision 13

Operations Monthly Performance Indicators, December 2007

Operations Quality Assurance Manual, dated December 13, 2007

OPEX Daily Report, January 29, 2008

Plant Modification Package - DCP/ECO #97-9075, Unit 1 Core Spray/RHR/LPCI Pressure

Switch Replacement, Revision 1

PL-NF-02-07, Channel Management Action Plan, Revision 28

Regulatory Guide 1.97, Criteria for Accident Monitoring Instrumentation, Revision 4

Specification Change Notice #6 for C-1056, Revision 3

Temporary Scaffold Log, dated January 15, 2008

Unit 1 & 2, Control Rod Drive Hydraulics System Health Report, May - August 2007

Unit 1, RHR Residual Heat Removal System Health Report, September - December 2007

Attachment

A-7

LIST OF ACRONYMS

ACE

Apparent Cause Evaluation

AR

Action Request

BWROG

Boiling Water Reactor Owners Group

CAP

Corrective Action Program

CAQ

Condition Adverse to Quality

CARB

Corrective Action Review Board

CFR

Code of Federal Regulations

CPG

Central Procedure Group

CR

Condition Report

CS

Core Spray

DBA

Design Basis Accident

DCP

Design Change Package

ECCS

Emergency Core Cooling System

ECP

Employee Concerns Program

EOP

Emergency Operating Procedures

EPG/SAG

Emergency Procedure Guidelines / Severe Accident Guidelines

EPU

Extended Power Uprate

FSAR

Final Safety Analysis Report

IMC

NRC Inspection Manual Chapter

LOCA

Loss of Coolant Accident

NCV

Non-Cited Violation

NRC

Nuclear Regulatory Commission

OE

Operating Experience

PAM

Post-Accident Monitoring

PI&R

Problem Identification and Resolution

psig

pounds per square inch

PSTG

Plant Specific Technical Guidelines

QA

Quality Assurance

RCA

Root Cause Analysis

RHR

Residual Heat Removal

ROP

Reactor Oversight Program

RPV

Reactor Pressure Vessel

SCWE

Safety Conscious Work Environment

SDP

Significance Determination Process

TS

Technical Specifications