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{{IR-Nav| site = 05000244 | year = 2002 | report number = 010 | {{Adams | ||
| number = ML023220481 | |||
| issue date = 11/18/2002 | |||
| title = IR 05000244-02-010, on 10/07/2002 - 10/25/2002, R. E. Ginna Nuclear Power Plant; Biennial Baseline Inspection of the Identification and Resolution of Problems | |||
| author name = Lew D | |||
| author affiliation = NRC/RGN-I/DRS/PEB | |||
| addressee name = Mecredy R | |||
| addressee affiliation = Rochester Gas & Electric Corp | |||
| docket = 05000244 | |||
| license number = DPR-018 | |||
| contact person = | |||
| document report number = IR-02-010 | |||
| document type = Inspection Report, Letter | |||
| page count = 16 | |||
}} | |||
{{IR-Nav| site = 05000244 | year = 2002 | report number = 010 }} | |||
=Text= | |||
{{#Wiki_filter:November 18, 2002 | |||
==SUBJECT:== | |||
GINNA - NRC PROBLEM IDENTIFICATION & RESOLUTION INSPECTION REPORT 50-244/02-010 | |||
==Dear Mr. Mecredy:== | |||
On October 25, 2002, the NRC completed a team inspection at the R. E. Ginna Facility. The enclosed inspection report documents the inspection findings, which were discussed with you and members of your staff during an exit meeting conducted on October 25, 2002. | |||
The inspection was an examination of activities conducted under your license as they related to the identification and resolution of problems, and compliance with the Commissions rules and regulations and the conditions of your operating license. Within these areas, the inspection involved examination of selected procedures and representative records, observations of activities, and interviews with personnel. | |||
On the basis of the sample selected for review, there were no findings of significance identified during this inspection. The team concluded that problems were properly identified, evaluated, and resolved withing the problem identification and resolution programs. However, during the inspection, several examples of minor problems were identified, including conditions adverse to quality that had not been entered into the corrective action program, narrowly focused Action Report evaluations, and some ineffective corrective actions. | |||
In accordance with 10CFR2.790 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web-site at http://www.nrc.gov/reading-rm/adams.html (the Public Reading Room). | |||
Sincerely, | |||
/RA/ | |||
David C. Lew, Chief Performance Evaluation Branch Division of Reactor Safety Docket No. | |||
50-244 License No. | |||
DPR-18 Enclosure: Inspection Report 50-244/02-010 cc w/encl: | |||
Dr. Robert | |||
=SUMMARY OF FINDINGS= | |||
IR 05000244/02-010; on October 7 - 25, 2002; R. E. Ginna Nuclear Power Plant; biennial baseline inspection of the identification and resolution of problems. | |||
The inspection was conducted by two regional inspectors and one contractor. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000. | |||
Identification and Resolution of Problems The team concluded that, in general, problems were properly identified, evaluated, and corrected. The licensees effectiveness at problem identification was acceptable overall. | |||
However, the NRC identified several minor deficiencies which were not identified or entered into the licensees corrective action system. While some minor exceptions were noted, the licensee adequately prioritized and evaluated problems that were entered into the corrective action program. Corrective actions, when specified, were generally implemented in a timely manner. | |||
Licensee audits and self-assessments were found to be adequate. On the basis of interviews conducted during this inspection, workers at the site felt free to input safety findings into the corrective action program. | |||
No findings of significance were identified. | |||
=REPORT DETAILS= | |||
==OTHER ACTIVITIES (OA)== | |||
{{a|4OA2}} | |||
==4OA2 Problem Identification and Resolution== | |||
a. | |||
Effectiveness of Problem Identification | |||
: (1) Inspection Scope The inspection team reviewed the procedures describing the corrective action process at the R. E. Ginna Nuclear Power Plant. The team reviewed a sample of action reports (AR) and deficiency tags to determine the threshold for identification of problems. The team reviewed logs, control room deficiencies and operator work-arounds, system health reports, work orders, temporary modifications, operating experience reviews, and procedures related to specific issues. In addition, the team interviewed staff and management to determine their understanding of the corrective action program. The specific documents reviewed and referenced during the inspection are listed in the attachment to this inspection report. | |||
The team reviewed a sample of quality assurance (QA) audits and surveillances, and departmental self-assessments in the areas of operations, maintenance, engineering, radiation protection, security, emergency preparedness, training, and the corrective action program itself. The review was to determine if assessment findings were entered into the corrective action program, and if the corrective actions were properly completed to resolve identified deficiencies. The team evaluated the effectiveness of the audits and self-assessments by comparing the associated results against self-revealing and NRC-identified findings. | |||
The team conducted several plant walk-downs of safety-related, risk significant areas to verify that observable system equipment and plant material adverse conditions were identified and entered into the corrective action program. The team also attended routine work control and management meetings to understand the interface between the corrective action program and the work control process. | |||
: (2) Findings Overall, the licensees effectiveness at problem identification was acceptable. The QA audits were self-critical and generally consistent with the teams findings. However, the team identified several minor deficiencies which were not identified or entered into the licensees corrective action system. Some examples for which the licensee subsequently initiated ARs are as follows. | |||
* The team found an auxiliary operators key ring lying on a structural support near a valve in the B diesel generator room. One of the keys on this ring operated locked valves and breakers throughout the plant. The key ring did not contain security or high radiation area keys, however, this set of keys was not identified as missing for about the one week they were subsequently determined to have been missing. The licensee initiated AR 2002-2272 in response to this discovery, and confirmed the proper alignment of components, as appropriate. | |||
* The team identified that the bend radius for one of the cables associated with the B safety-related battery was smaller than the acceptance limit. This particular cable was notably shorter in length than other battery cables. The operability of the battery was not impacted, however, the configuration did not conform to the design and installation criterion (AR 2002-2283 written). | |||
The team also identified several other minor problems, such as implementation problems associated with the classification and storage of Precursor reports (for events of very low significance that require no investigative or corrective action); a small amount of boric acid on a safety injection system instrument fitting; and the presence of a screen covering the open end of the standby auxiliary feedwater test tank vent, contrary to the associated drawing. Regarding the details associated with the uncontrolled key ring described above, the team identified some broader concerns relative to key control and accountability. Inventory control for this type of key set, as well as other keys controlled by operations, was weak. There were prior individual key control deficiencies that had been identified via ARs (2001-1325 and 2001-1325), but the lack of an effective key control program was not recognized or addressed. As indicated by the noted examples, the team concluded that the licensee exhibited some weaknesses with regard to problem identification. | |||
b. | |||
Prioritization and Evaluation of Issues | |||
: (1) Inspection Scope The team reviewed the ARs and work orders listed in the attachment to this report to assess whether the licensee adequately prioritized and evaluated the identified problems. This review included the causal assessment of each issue (e.g., a root cause analysis or an apparent cause evaluation); and for significant conditions adverse to quality, the extent of condition and determination of corrective actions to preclude recurrence. The team also evaluated the ARs for potential impact on equipment or system operability, reliability or unavailability. | |||
The team reviewed the backlog of operations, maintenance and engineering issues to determine if issues were properly prioritized, and if individually or collectively, they represented an increased risk due to the delay of corrective actions. The team also reviewed the status and plans to correct equipment problems identified in system health reports and the Maintenance Rule documents. The team attended the daily screening and management meetings to evaluate the licensees ability to assess AR significance and identify if the initial determination of operability and reportability were correct. | |||
The team observed portions of the onsite Plant Operations Review Committee (PORC)and the offsite Nuclear Safety Audit Review Board (NSARB), and reviewed the minutes of past meetings, to determine if the associated reviews were critical of the sites activities. | |||
: (2) Findings The team concluded that, in general, the licensee adequately prioritized and evaluated the issues and concerns entered into the AR process. Operability and reportability determinations were accurately performed in a timely fashion. Overall, the root cause analyses reviewed were thorough, determined the root cause and contributing causes, and recommended corrective actions that correlated to the identified causes. As required, corrective actions were generally identified and implemented to preclude recurrence for significant conditions adverse to quality. The overall backlog of issues appeared reasonable and properly evaluated for risk. | |||
Notwithstanding the overall acceptable performance in this area, the team identified some minor instances where the Ginna staff had not properly prioritized or evaluated conditions adverse to quality. These examples are described as follows. | |||
* AR 2002-0613 discussed a plant configuration where three of the five possible make-up paths were isolated from the reactor coolant system (RCS) while in a reduced inventory condition. This issue was previously characterized as a non-cited violation for the failure to follow procedures. During this inspection, the team noted the following with respect to the AR: 1) the event was not considered to be a Significant Condition Adverse to Quality; 2) the AR was prioritized improperly low as a Priority 3 with an evaluation due date in June 2002; 3) the AR was improperly determined to be non-consequential from a human impact consideration; and (4)an Extension Request was submitted and approved to extend the investigation completion date to November 2002, which would be about eight months after the event. The extension basis focused on clarifying the valve line-up procedures; and the safety significance was noted as None as the licensee considered this to be only a refueling outage concern. | |||
The team determined the licensees actions taken to date and planned addressed the specific valve issue and not the human performance nature of why the Work Control Supervisor allowed the tags to be hung. Also, the team judged that the licensees event classification, prioritization, and human impact consideration minimized the potential safety impact. A more appropriate characterization likely would have necessitated a more rigorous and timely root cause analysis. Further, while the AR noted that an apparent cause was to be performed for a human performance event, the evaluation had not been completed as of the time of this inspection. Because the human performance causal analysis was not yet completed in a timely manner, the potential exists that relevant information may not be captured or recalled. Finally, the team considered the original issue to be a Significant Condition Adverse to Quality because it resulted in a reduced number of available make-up sources designed to mitigate the consequences of a draindown event while already in a reduced RCS inventory configuration. Although a similar or repeat occurrence had not resulted due to the ineffective processing and evaluation (including corrective actions) of this AR, the team concluded that the licensees overall response to this condition did not display a conservative safety focus. The licensee initiated AR 2002-2427 to address these concerns. | |||
* In some cases, the priority level was not in alignment with event significance and procedure guidance. For example, AR 2002-2097 involved an equipment problem that resulted in a reactivity excursion (99.5% to slightly greater than 100%) due to an unexpected dilution, but was assigned Priority 4 (trending). Consistent with the guidance provided in procedure IP-NPD-4, Nuclear Operations Group Work Prioritization, it should have been Priority 2 (unexpected reactivity excursion such as a significant dilution). The team concluded that although the priority was incorrect, the licensee adequately evaluated and corrected the associated condition. | |||
The licensee initiated AR 2002-2461 to address the incorrect priority assignment. | |||
* The team concluded that AR evaluations involving human performance appeared less detailed and probing than those evaluations involving equipment performance. | |||
As an example, AR 2002-1809 (diesel generator breaker closed out of phase during testing) emphasized process and procedure weaknesses and enhancements over the potential human performance problems (e.g., self-check techniques, supervisory oversight). | |||
c. | |||
Effectiveness of Corrective Actions | |||
: (1) Inspection Scope The team reviewed the corrective actions associated with selected ARs to determine whether the actions had addressed the identified causes of the problems. The team also reviewed the licensees timeliness for implementing the corrective actions, and their effectiveness in precluding recurrence for significant conditions adverse to quality. The team also reviewed the non-cited violations issued since the last inspection of the Ginna corrective action program to determine if issues placed in their program had been properly evaluated and corrected. | |||
: (2) Findings Overall, the inspectors determined that corrective actions associated with ARs were effective; and as applicable, corrective actions were adequate to prevent problem recurrence (for significant conditions adverse to quality). The team found that, in general, the corrective actions were completed or scheduled to be completed in a timely manner commensurate with the significance of the issue. The team did not identify corrective actions in the backlog of work that represented an adverse impact on safety. | |||
Notwithstanding, the team identified some minor instances where the licensees corrective actions were weak, and examples are described below. | |||
* In a period of less than two years, there were four occurrences where service air header pressure was decreased due to the use of an air-operated vacuum cleaner. This was an undesirable condition that could potentially challenge the instrument air system, which is normally cross-connected to service air and provides motive force for several safety and risk significant systems (e.g., main steam isolation valves and feedwater regulating valves). Some of the licensees corrective actions included various administrative controls to ensure that personnel split the service and instrument air headers (prior to using the vacuum). However, these actions were repeatedly ineffective until the licensee implemented a corrective action to lock the vacuum cleaner, with the key in the control of the Shift Supervisor. The team determined that the use of the vacuum cleaner had not caused a plant transient, and neither the service air nor the instrument air system is safety related. Thus the failure to implement effective corrective actions was not a violation of NRC regulations. However, the lack of effective actions for these occurrences was noteworthy because the condition could have contributed to or caused a plant transient. The licensee initiated AR 2002-2428 in response to these concerns. | |||
* Several ARs have been initiated following NRCs identification of deficiencies associated with tracking equipment unavailability time for the NRC performance indicators (PI). The errors were minor in nature and magnitude, and none of the errors would have changed the affected PI color (threshold). However, the team determined that the licensees actions to date have not been effective in preventing continued errors (AR 2002-2463 written). | |||
d. Assessment of Safety Conscious Work Environment | |||
: (1) Inspection Scope During the inspection, the team interviewed plant staff to determine if conditions existed at the site which would result in personnel being hesitant to raise safety concerns to Ginna management and/or the NRC. | |||
: (2) Findings No findings of significance were identified. | |||
{{a|4OA6}} | |||
==4OA6 Meetings== | |||
a. | |||
===Exit Meeting Summary=== | |||
On October 25, 2002, the team presented the inspection results to Dr. R. Mecredy and members of his staff. During the inspection, no proprietary material was examined or retained by the team. | |||
: | |||
Partial List of Persons Contacted Items Opened & Closed List of Documents Reviewed List of Acronyms | |||
1 of 6 ATTACHMENT A. | |||
PARTIAL LIST OF PERSONS CONTACTED RG&E: | |||
P. Bamford Manager, Operations M. Flaherty Manager, Nuclear Safety & Licensing R. Forgensi Manager, Operational Review J. | |||
Germain Operational Review Analysis T. Harding Licensing Engineer J. | |||
Hotchkiss Manager, Mechanical Maintenance T. Laursen Manager, Emergency Preparedness & Training Support M. Lilley Manager, Quality Assurance R. Marchionda Department Manager, Nuclear Assessment K. McCarthy Operational Review Engineer R. McMahon Operating Experience Engineer R. Mecredy Vice President, Nuclear Operations T. Miller System Engineer N. Olivia Senior Electrical Engineer P. Polfleit Corporate Nuclear Emergency Planner M. Ruby Licensing Engineer M. Smith System Engineer L. Stavalone Trending Analyst R. Teed Manager - Nuclear Security R. Watts Department Manager, Nuclear Training J. | |||
Wayland Manager, I&C/Electrical Maintenance T. White Manager, Balance of Plant Systems J. | |||
Zapetis Maintenance Rule Coordinator NRC: | |||
K. Kolaczyk Senior Resident Inspector, Ginna D. Lew Branch Chief, Performance Evaluation Branch, Region I C. Welch Resident Inspector, Ginna B. | |||
ITEMS OPENED & CLOSED None (cont.) | |||
2 of 6 C. | |||
LIST OF | |||
=DOCUMENTS REVIEWED= | |||
Procedures: | |||
Plant Operations Review Committee Operating Procedure, Rev. 53 | |||
AP-RCP.1 | |||
Reactor Coolant Pump Seal Malfunction, Rev. 14 | |||
AR-AA-3 | |||
Alarm Response Procedure - Standby AFW Tank, Rev. 6 | |||
AR-B-17 | |||
Alarm Response Procedure - Seal Flow, Rev. 12 | |||
EP-2-P-0168 | |||
Maintenance Rule Monitoring, Rev. 5 | |||
FR-C.2 | |||
Response to Degraded Core Cooling, Rev. 16 | |||
FR-H.1 | |||
Response to Loss of Secondary Heat Sink, Rev. 27 | |||
FR-I.3 | |||
Response to Voids in Reactor Vessel, Rev. 16 | |||
GC-76.10 | |||
Installation, Testing and Inspection of Wire and Cable, Rev. 5 | |||
IP-CAP-1 | |||
Abnormal Condition Tracking Initiation or Notification (Action) Report, | |||
Rev. 14 | |||
IP-DES-1 | |||
Technical Staff Request, Rev. 3 | |||
IP-IIT-5 | |||
Snubber Inspection and Testing Program, Rev. 1 | |||
IP-NPD-4 | |||
Nuclear Operations Group Work Prioritization, Rev. 6 | |||
IP-NPD-6 | |||
Nuclear Safety Audit and Review Board (NSARB), Rev. 4 | |||
IP-RDM-3 | |||
Ginna Records, Rev. 5 | |||
IP-SEP-2 | |||
Self Assessment, Rev. 4 | |||
IP-SEP-3 | |||
Ginna Station Management Observation, Coaching and Tours | |||
Program, Rev. 2 | |||
S-16.13 | |||
RWST Water Makeup to Accumulators, Rev. 30 | |||
T-44.1 | |||
Condensate Test Tank for Standby AFW Pumps Filling or Draining, | |||
Rev. 17 | |||
A-1603.0 | |||
Overview of the Ginna Station Work Control System, Revision 19 | |||
A-1603.1 | |||
Work Request / Trouble Report Initiation, Revision 14 | |||
A-1603.2 | |||
Work Order Initiation, Revision 15 | |||
A-1603.6 | |||
Post Maintenance / Modification Testing, Revision 8 | |||
A-1603.8 | |||
Work Order Processing for Emergency and/or After Hours | |||
Maintenance, Revision 7 | |||
2.12 | |||
Inoperability of Equipment Important to a Safety, Revision 41 | |||
2.4 | |||
Control of Limiting Conditions for Operating Equipment, Revision 119 | |||
G-ORS-01 | |||
Screening Committee Guideline, Revision 50 | |||
IP-CAP-1.1 | |||
Operability and Past Operability Determination Checklist, Revision 2 | |||
IP-CAP-1.4 | |||
AR Extension Request, Revision 1 | |||
IP-CAP-1.8 | |||
Effectiveness Review Form, Revision 0 | |||
IP-CAP-2 | |||
Root Cause Analysis for Equipment Failures, Revision 4 | |||
IP-CAP-4 | |||
Problem Solving, Revision 1 | |||
IP-CAP-5 | |||
Event Trending Process, Revision 1 | |||
IP-CAP-6 | |||
10CFR021 Screening, Evaluating, and Reporting, Revision 2 | |||
IP-HPE-1 | |||
Human Performance Event Evaluation Process, Revision 3 | |||
IP-NPD-4 | |||
Nuclear Operations Group Work Prioritization, Revision 6 | |||
IP-PSH-1 | |||
Integrated Work Schedule, Revision 6 | |||
IP-PSH-2 | |||
Integrated Work Schedule Risk Management, Revision 6 | |||
OP-2.3.1 | |||
Draining & Operation at Reduced Inventory of the Reactor Coolant | |||
System, Revision 71 | |||
SPG-02 | |||
Integrated Work Schedule Schedulers Handbook, Revision 11 | |||
(cont.) | |||
of 6 | |||
Non-Cited Violations: | |||
NCV 2001-06-01 | |||
Failure to Perform Flow Rate Determinations as per ODCM | |||
NCV 2001-08-01 | |||
Failure to Include Acceptance Criteria in Procedures | |||
NCV 2001-08-02 | |||
Failure to Implement MSIV Surveillance Requirement | |||
NCV 2001-09-01 | |||
Inappropriate Procedures During Service Water Pump Motor | |||
Replacement | |||
NCV 2001-10-01 | |||
Failure to Identify Seismic Issue with Containment Isolation Valve | |||
NCV 2002-02-01 | |||
RCS Make-up Flow Paths Were Inappropriately Isolated | |||
NCV 2002-02-02 | |||
Improper Source Range Detector Calibration | |||
NCV 2002-03-01 | |||
Failure to Control/Evaluate Compensatory Fire Protection Measure | |||
NCV 2002-03-02 | |||
Unlocked Technical Specification High Radiation Area | |||
NCV 2002-09-01 | |||
Failure to Utilize Mobile Loudspeakers for Transient Population | |||
NCV 2001-09-02 | |||
Failure to Correct Equipment & Human Performance Problems | |||
Quality Assurance Audits: | |||
2000-0014-BKS | |||
Corrective Action & Operating Experience Programs | |||
2001-0004-DHK | |||
Emergency Response Plan | |||
2001-0009-JMT | |||
Engineering and Configuration Control Audit | |||
2001-0010-RTD | |||
Problem Identification and Resolution Process Audit | |||
2001-0013-TGT | |||
Operations Audit | |||
2001-0017-PJH | |||
Audit of Ginna Station Technical Specifications | |||
2002-0001-JMT | |||
ODCM and REMP Audit | |||
2002-0002-TGT | |||
Maintenance Audit | |||
2002-0003-BKS | |||
Cooperative Management Assessment Program | |||
2002-0004-RTD | |||
Emergency Preparedness Audit | |||
2002-0006-DHK | |||
Radiation Protection Audit | |||
Self-Assessments: | |||
2001-0025 | |||
Corrective Action Process Effectiveness | |||
2002-0023 | |||
Effectiveness of Corrective Actions for Areas for Improvement | |||
Identified During January 2001 Self-Evaluation | |||
2002-0031 | |||
Effectiveness Review of Contamination Control During Reactor | |||
Cavity Decontamination | |||
2002-0041 | |||
Quality Control Program Preparedness | |||
2002-0042 | |||
Self-Assessment of NCV Related to Reduced Inventory | |||
2002-0043 | |||
Self-Assessment of NCV Related to the Alert Notification System | |||
(cont.) | |||
of 6 | |||
Action Reports: (* Denotes CR generated as a result of this inspection; P denotes a Precursor Report) | |||
1997-1447 | |||
2000-0188 | |||
2000-1176 | |||
2000-1268 | |||
2000-1301 | |||
2000-1489 | |||
2000-1630 | |||
2001-0001P | |||
2001-0013P | |||
2001-0131P | |||
2001-0141P | |||
2001-0326P | |||
2001-0393P | |||
2001-0457P | |||
2001-0517P | |||
2001-0676 | |||
2001-0740P | |||
2001-0783 | |||
2001-0862 | |||
2001-0923 | |||
2001-1070P | |||
2001-1148 | |||
2001-1325 | |||
2001-1341 | |||
2001-1365 | |||
2001-1395 | |||
2001-1465 | |||
2001-1632 | |||
2001-1691 | |||
2001-1702 | |||
2001-1749 | |||
2001-1757 | |||
2001-1764 | |||
2001-1767 | |||
2001-1774 | |||
2001-1802 | |||
2001-1840 | |||
2001-1867 | |||
2001-1879 | |||
2001-1888 | |||
2001-1921 | |||
2001-1921 | |||
2001-1943 | |||
2001-1969 | |||
2001-2091 | |||
2001-2131 | |||
2001-2140 | |||
2001-2227 | |||
2001-2245 | |||
2001-2245 | |||
2001-4355 | |||
2002-0038 | |||
2002-0070 | |||
2002-0101 | |||
2002-0109 | |||
2002-0126 | |||
2002-0127 | |||
2002-0142 | |||
2002-0150P | |||
2002-0161 | |||
2002-0163 | |||
2002-0193 | |||
2002-0193 | |||
2002-0195 | |||
2002-0195 | |||
2002-0237P | |||
2002-0244P | |||
2002-0266 | |||
2002-0371 | |||
2002-0371 | |||
2002-0417 | |||
2002-0421 | |||
2002-0479 | |||
2002-0492 | |||
2002-0530 | |||
2002-0530 | |||
2002-0530 | |||
2002-0538 | |||
2002-0541 | |||
2002-0595P | |||
2002-0661 | |||
2002-0670P | |||
2002-0730P | |||
2002-0756 | |||
2002-0766 | |||
2002-0821 | |||
2002-0822 | |||
2002-0878 | |||
2002-0904 | |||
2002-0931 | |||
2002-0948 | |||
2002-0976 | |||
2002-1014 | |||
2002-1022 | |||
2002-1028 | |||
2002-1028 | |||
2002-1146 | |||
2002-1146 | |||
2002-1149 | |||
2002-1151 | |||
2002-1151 | |||
2002-1170 | |||
2002-1202 | |||
2002-1362 | |||
2002-1508 | |||
2002-1564 | |||
2002-1593 | |||
2002-1596 | |||
2002-1634 | |||
2002-1663 | |||
2002-1753 | |||
2002-1759 | |||
2002-1770 | |||
2002-1809 | |||
2002-1849 | |||
2002-1941 | |||
2002-1997 | |||
2002-2035 | |||
2002-2035 | |||
2002-2060 | |||
2002-2097 | |||
2002-2116 | |||
2002-2260 | |||
2002-2261 | |||
2002-2271* | |||
2002-2272* | |||
2002-2273* | |||
2002-2277 | |||
2002-2283* | |||
2002-2286* | |||
2002-2287* | |||
2002-2288* | |||
2002-2289* | |||
2002-2290* | |||
2002-2300* | |||
2002-2303* | |||
2002-2304* | |||
2002-2308* | |||
2002-2309* | |||
2002-2311* | |||
2002-2405 | |||
2002-2405* | |||
2002-2411* | |||
Work Orders: | |||
WO-20103571 Repair Lug Crimps on the B Service Water Pump | |||
WO-20103583 Repair Lug Crimps on the A, C, & D Service Water Pumps | |||
WO-20200848 Trouble shoot and repair AOV-371, Indicates Mid-Position but 25% | |||
Open (related to AR 2002-0756) | |||
WO-20201827 Repair A Containment Sump Pump Level Switch (LS-2039) | |||
WO-20202034 Operations Suspects That V-214 Leaks By | |||
WO-20202266 Install PCR 2002-0027, Replace Emergency Siren System | |||
WO-20202387 Reach Rod to V-214 Needs to Be Replaced | |||
(cont.) | |||
of 6 | |||
Miscellaneous Documents: | |||
PORC Meeting Minutes for meetings 2001-0041; 2001-0042; 2001-0049; 2002-0004; | |||
2002-0007; 2002-0014; 2002-0021; 2002-0024; 2002-0028; 2002-0035; 2002-0040; | |||
2002-0042; 2002-0045; 2002-0048 | |||
Nuclear Safety Audit Review Board (NSRB) Minutes for meetings 243, 244, and 245 | |||
Modification PCR-2002-0012, Relocate the Siren Central Control Unit to Ginna | |||
Modification PCR-2002-0027, Replace Emergency Siren System | |||
Temporary Modification 2000-0007, A S/G Blow-down Corrosion Product Sampler, | |||
Rev. 1 | |||
Temporary Modification 2001-0012, Temporary SI Accumulator Makeup Pump, Rev. 1 | |||
Updated Final Safety Analysis Report | |||
5059SCRN-2002-0524, Replace Emergency Siren System (related to WO-20202266) | |||
Maintenance Department Monthly Performance Indicator Report (i.e. - backlog), | |||
September 2002 | |||
Nuclear Emergency Response Plan, Revision 20 | |||
ProActive Assessment of Workplace Factors (PAOWF), August 2002 | |||
(cont.) | |||
of 6 | |||
D. | |||
ACRONYMS | |||
ADAMS Agencywide Documents Access and Management System | |||
AFW | |||
Auxiliary Feedwater | |||
AOV | |||
Air Operated Valve | |||
AR | |||
Action Report | |||
CFR | |||
Code of Federal Regulations | |||
EDG | |||
Emergency Diesel Generator | |||
I&C | |||
Instruments & Controls | |||
MSIV | |||
Main Steam Isolation Valve | |||
NCV | |||
Non-Cited Violation | |||
NRC | |||
Nuclear Regulatory Commission | |||
NSARB Nuclear Safety Audit Review Board | |||
ODCM | |||
Offsite Dose Calculation Manual | |||
PAOWF ProActive Assessment of Workplace Factors | |||
PARS | |||
Publicly Available Records System | |||
PCR | |||
Plant Change Request | |||
PI | |||
Performance Indicator | |||
PORC | |||
Plant Operations Review Committee | |||
QA | |||
Quality Assurance | |||
RCS | |||
Reactor Coolant System | |||
REMP | |||
Radiological Environmental Monitoring Program | |||
RG&E | |||
Rochester Gas and Electric Corporation | |||
RWST | |||
Reactor Water Storage Tank | |||
SDP | |||
Significance Determination Process | |||
TM | |||
Temporary Modification | |||
TS | |||
Technical Specification | |||
WO | |||
Work Order | |||
}} | |||
Latest revision as of 14:21, 16 January 2025
| ML023220481 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 11/18/2002 |
| From: | David Lew NRC/RGN-I/DRS/PEB |
| To: | Mecredy R Rochester Gas & Electric Corp |
| References | |
| IR-02-010 | |
| Download: ML023220481 (16) | |
Text
November 18, 2002
SUBJECT:
GINNA - NRC PROBLEM IDENTIFICATION & RESOLUTION INSPECTION REPORT 50-244/02-010
Dear Mr. Mecredy:
On October 25, 2002, the NRC completed a team inspection at the R. E. Ginna Facility. The enclosed inspection report documents the inspection findings, which were discussed with you and members of your staff during an exit meeting conducted on October 25, 2002.
The inspection was an examination of activities conducted under your license as they related to the identification and resolution of problems, and compliance with the Commissions rules and regulations and the conditions of your operating license. Within these areas, the inspection involved examination of selected procedures and representative records, observations of activities, and interviews with personnel.
On the basis of the sample selected for review, there were no findings of significance identified during this inspection. The team concluded that problems were properly identified, evaluated, and resolved withing the problem identification and resolution programs. However, during the inspection, several examples of minor problems were identified, including conditions adverse to quality that had not been entered into the corrective action program, narrowly focused Action Report evaluations, and some ineffective corrective actions.
In accordance with 10CFR2.790 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web-site at http://www.nrc.gov/reading-rm/adams.html (the Public Reading Room).
Sincerely,
/RA/
David C. Lew, Chief Performance Evaluation Branch Division of Reactor Safety Docket No.
50-244 License No.
DPR-18 Enclosure: Inspection Report 50-244/02-010 cc w/encl:
Dr. Robert
SUMMARY OF FINDINGS
IR 05000244/02-010; on October 7 - 25, 2002; R. E. Ginna Nuclear Power Plant; biennial baseline inspection of the identification and resolution of problems.
The inspection was conducted by two regional inspectors and one contractor. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
Identification and Resolution of Problems The team concluded that, in general, problems were properly identified, evaluated, and corrected. The licensees effectiveness at problem identification was acceptable overall.
However, the NRC identified several minor deficiencies which were not identified or entered into the licensees corrective action system. While some minor exceptions were noted, the licensee adequately prioritized and evaluated problems that were entered into the corrective action program. Corrective actions, when specified, were generally implemented in a timely manner.
Licensee audits and self-assessments were found to be adequate. On the basis of interviews conducted during this inspection, workers at the site felt free to input safety findings into the corrective action program.
No findings of significance were identified.
REPORT DETAILS
OTHER ACTIVITIES (OA)
4OA2 Problem Identification and Resolution
a.
Effectiveness of Problem Identification
- (1) Inspection Scope The inspection team reviewed the procedures describing the corrective action process at the R. E. Ginna Nuclear Power Plant. The team reviewed a sample of action reports (AR) and deficiency tags to determine the threshold for identification of problems. The team reviewed logs, control room deficiencies and operator work-arounds, system health reports, work orders, temporary modifications, operating experience reviews, and procedures related to specific issues. In addition, the team interviewed staff and management to determine their understanding of the corrective action program. The specific documents reviewed and referenced during the inspection are listed in the attachment to this inspection report.
The team reviewed a sample of quality assurance (QA) audits and surveillances, and departmental self-assessments in the areas of operations, maintenance, engineering, radiation protection, security, emergency preparedness, training, and the corrective action program itself. The review was to determine if assessment findings were entered into the corrective action program, and if the corrective actions were properly completed to resolve identified deficiencies. The team evaluated the effectiveness of the audits and self-assessments by comparing the associated results against self-revealing and NRC-identified findings.
The team conducted several plant walk-downs of safety-related, risk significant areas to verify that observable system equipment and plant material adverse conditions were identified and entered into the corrective action program. The team also attended routine work control and management meetings to understand the interface between the corrective action program and the work control process.
- (2) Findings Overall, the licensees effectiveness at problem identification was acceptable. The QA audits were self-critical and generally consistent with the teams findings. However, the team identified several minor deficiencies which were not identified or entered into the licensees corrective action system. Some examples for which the licensee subsequently initiated ARs are as follows.
- The team found an auxiliary operators key ring lying on a structural support near a valve in the B diesel generator room. One of the keys on this ring operated locked valves and breakers throughout the plant. The key ring did not contain security or high radiation area keys, however, this set of keys was not identified as missing for about the one week they were subsequently determined to have been missing. The licensee initiated AR 2002-2272 in response to this discovery, and confirmed the proper alignment of components, as appropriate.
- The team identified that the bend radius for one of the cables associated with the B safety-related battery was smaller than the acceptance limit. This particular cable was notably shorter in length than other battery cables. The operability of the battery was not impacted, however, the configuration did not conform to the design and installation criterion (AR 2002-2283 written).
The team also identified several other minor problems, such as implementation problems associated with the classification and storage of Precursor reports (for events of very low significance that require no investigative or corrective action); a small amount of boric acid on a safety injection system instrument fitting; and the presence of a screen covering the open end of the standby auxiliary feedwater test tank vent, contrary to the associated drawing. Regarding the details associated with the uncontrolled key ring described above, the team identified some broader concerns relative to key control and accountability. Inventory control for this type of key set, as well as other keys controlled by operations, was weak. There were prior individual key control deficiencies that had been identified via ARs (2001-1325 and 2001-1325), but the lack of an effective key control program was not recognized or addressed. As indicated by the noted examples, the team concluded that the licensee exhibited some weaknesses with regard to problem identification.
b.
Prioritization and Evaluation of Issues
- (1) Inspection Scope The team reviewed the ARs and work orders listed in the attachment to this report to assess whether the licensee adequately prioritized and evaluated the identified problems. This review included the causal assessment of each issue (e.g., a root cause analysis or an apparent cause evaluation); and for significant conditions adverse to quality, the extent of condition and determination of corrective actions to preclude recurrence. The team also evaluated the ARs for potential impact on equipment or system operability, reliability or unavailability.
The team reviewed the backlog of operations, maintenance and engineering issues to determine if issues were properly prioritized, and if individually or collectively, they represented an increased risk due to the delay of corrective actions. The team also reviewed the status and plans to correct equipment problems identified in system health reports and the Maintenance Rule documents. The team attended the daily screening and management meetings to evaluate the licensees ability to assess AR significance and identify if the initial determination of operability and reportability were correct.
The team observed portions of the onsite Plant Operations Review Committee (PORC)and the offsite Nuclear Safety Audit Review Board (NSARB), and reviewed the minutes of past meetings, to determine if the associated reviews were critical of the sites activities.
- (2) Findings The team concluded that, in general, the licensee adequately prioritized and evaluated the issues and concerns entered into the AR process. Operability and reportability determinations were accurately performed in a timely fashion. Overall, the root cause analyses reviewed were thorough, determined the root cause and contributing causes, and recommended corrective actions that correlated to the identified causes. As required, corrective actions were generally identified and implemented to preclude recurrence for significant conditions adverse to quality. The overall backlog of issues appeared reasonable and properly evaluated for risk.
Notwithstanding the overall acceptable performance in this area, the team identified some minor instances where the Ginna staff had not properly prioritized or evaluated conditions adverse to quality. These examples are described as follows.
- AR 2002-0613 discussed a plant configuration where three of the five possible make-up paths were isolated from the reactor coolant system (RCS) while in a reduced inventory condition. This issue was previously characterized as a non-cited violation for the failure to follow procedures. During this inspection, the team noted the following with respect to the AR: 1) the event was not considered to be a Significant Condition Adverse to Quality; 2) the AR was prioritized improperly low as a Priority 3 with an evaluation due date in June 2002; 3) the AR was improperly determined to be non-consequential from a human impact consideration; and (4)an Extension Request was submitted and approved to extend the investigation completion date to November 2002, which would be about eight months after the event. The extension basis focused on clarifying the valve line-up procedures; and the safety significance was noted as None as the licensee considered this to be only a refueling outage concern.
The team determined the licensees actions taken to date and planned addressed the specific valve issue and not the human performance nature of why the Work Control Supervisor allowed the tags to be hung. Also, the team judged that the licensees event classification, prioritization, and human impact consideration minimized the potential safety impact. A more appropriate characterization likely would have necessitated a more rigorous and timely root cause analysis. Further, while the AR noted that an apparent cause was to be performed for a human performance event, the evaluation had not been completed as of the time of this inspection. Because the human performance causal analysis was not yet completed in a timely manner, the potential exists that relevant information may not be captured or recalled. Finally, the team considered the original issue to be a Significant Condition Adverse to Quality because it resulted in a reduced number of available make-up sources designed to mitigate the consequences of a draindown event while already in a reduced RCS inventory configuration. Although a similar or repeat occurrence had not resulted due to the ineffective processing and evaluation (including corrective actions) of this AR, the team concluded that the licensees overall response to this condition did not display a conservative safety focus. The licensee initiated AR 2002-2427 to address these concerns.
- In some cases, the priority level was not in alignment with event significance and procedure guidance. For example, AR 2002-2097 involved an equipment problem that resulted in a reactivity excursion (99.5% to slightly greater than 100%) due to an unexpected dilution, but was assigned Priority 4 (trending). Consistent with the guidance provided in procedure IP-NPD-4, Nuclear Operations Group Work Prioritization, it should have been Priority 2 (unexpected reactivity excursion such as a significant dilution). The team concluded that although the priority was incorrect, the licensee adequately evaluated and corrected the associated condition.
The licensee initiated AR 2002-2461 to address the incorrect priority assignment.
- The team concluded that AR evaluations involving human performance appeared less detailed and probing than those evaluations involving equipment performance.
As an example, AR 2002-1809 (diesel generator breaker closed out of phase during testing) emphasized process and procedure weaknesses and enhancements over the potential human performance problems (e.g., self-check techniques, supervisory oversight).
c.
Effectiveness of Corrective Actions
- (1) Inspection Scope The team reviewed the corrective actions associated with selected ARs to determine whether the actions had addressed the identified causes of the problems. The team also reviewed the licensees timeliness for implementing the corrective actions, and their effectiveness in precluding recurrence for significant conditions adverse to quality. The team also reviewed the non-cited violations issued since the last inspection of the Ginna corrective action program to determine if issues placed in their program had been properly evaluated and corrected.
- (2) Findings Overall, the inspectors determined that corrective actions associated with ARs were effective; and as applicable, corrective actions were adequate to prevent problem recurrence (for significant conditions adverse to quality). The team found that, in general, the corrective actions were completed or scheduled to be completed in a timely manner commensurate with the significance of the issue. The team did not identify corrective actions in the backlog of work that represented an adverse impact on safety.
Notwithstanding, the team identified some minor instances where the licensees corrective actions were weak, and examples are described below.
- In a period of less than two years, there were four occurrences where service air header pressure was decreased due to the use of an air-operated vacuum cleaner. This was an undesirable condition that could potentially challenge the instrument air system, which is normally cross-connected to service air and provides motive force for several safety and risk significant systems (e.g., main steam isolation valves and feedwater regulating valves). Some of the licensees corrective actions included various administrative controls to ensure that personnel split the service and instrument air headers (prior to using the vacuum). However, these actions were repeatedly ineffective until the licensee implemented a corrective action to lock the vacuum cleaner, with the key in the control of the Shift Supervisor. The team determined that the use of the vacuum cleaner had not caused a plant transient, and neither the service air nor the instrument air system is safety related. Thus the failure to implement effective corrective actions was not a violation of NRC regulations. However, the lack of effective actions for these occurrences was noteworthy because the condition could have contributed to or caused a plant transient. The licensee initiated AR 2002-2428 in response to these concerns.
- Several ARs have been initiated following NRCs identification of deficiencies associated with tracking equipment unavailability time for the NRC performance indicators (PI). The errors were minor in nature and magnitude, and none of the errors would have changed the affected PI color (threshold). However, the team determined that the licensees actions to date have not been effective in preventing continued errors (AR 2002-2463 written).
d. Assessment of Safety Conscious Work Environment
- (1) Inspection Scope During the inspection, the team interviewed plant staff to determine if conditions existed at the site which would result in personnel being hesitant to raise safety concerns to Ginna management and/or the NRC.
- (2) Findings No findings of significance were identified.
4OA6 Meetings
a.
Exit Meeting Summary
On October 25, 2002, the team presented the inspection results to Dr. R. Mecredy and members of his staff. During the inspection, no proprietary material was examined or retained by the team.
Partial List of Persons Contacted Items Opened & Closed List of Documents Reviewed List of Acronyms
1 of 6 ATTACHMENT A.
PARTIAL LIST OF PERSONS CONTACTED RG&E:
P. Bamford Manager, Operations M. Flaherty Manager, Nuclear Safety & Licensing R. Forgensi Manager, Operational Review J.
Germain Operational Review Analysis T. Harding Licensing Engineer J.
Hotchkiss Manager, Mechanical Maintenance T. Laursen Manager, Emergency Preparedness & Training Support M. Lilley Manager, Quality Assurance R. Marchionda Department Manager, Nuclear Assessment K. McCarthy Operational Review Engineer R. McMahon Operating Experience Engineer R. Mecredy Vice President, Nuclear Operations T. Miller System Engineer N. Olivia Senior Electrical Engineer P. Polfleit Corporate Nuclear Emergency Planner M. Ruby Licensing Engineer M. Smith System Engineer L. Stavalone Trending Analyst R. Teed Manager - Nuclear Security R. Watts Department Manager, Nuclear Training J.
Wayland Manager, I&C/Electrical Maintenance T. White Manager, Balance of Plant Systems J.
Zapetis Maintenance Rule Coordinator NRC:
K. Kolaczyk Senior Resident Inspector, Ginna D. Lew Branch Chief, Performance Evaluation Branch, Region I C. Welch Resident Inspector, Ginna B.
ITEMS OPENED & CLOSED None (cont.)
2 of 6 C.
LIST OF
DOCUMENTS REVIEWED
Procedures:
Plant Operations Review Committee Operating Procedure, Rev. 53
AP-RCP.1
Reactor Coolant Pump Seal Malfunction, Rev. 14
Alarm Response Procedure - Standby AFW Tank, Rev. 6
AR-B-17
Alarm Response Procedure - Seal Flow, Rev. 12
EP-2-P-0168
Maintenance Rule Monitoring, Rev. 5
FR-C.2
Response to Degraded Core Cooling, Rev. 16
FR-H.1
Response to Loss of Secondary Heat Sink, Rev. 27
FR-I.3
Response to Voids in Reactor Vessel, Rev. 16
GC-76.10
Installation, Testing and Inspection of Wire and Cable, Rev. 5
IP-CAP-1
Abnormal Condition Tracking Initiation or Notification (Action) Report,
Rev. 14
IP-DES-1
Technical Staff Request, Rev. 3
IP-IIT-5
Snubber Inspection and Testing Program, Rev. 1
IP-NPD-4
Nuclear Operations Group Work Prioritization, Rev. 6
IP-NPD-6
Nuclear Safety Audit and Review Board (NSARB), Rev. 4
IP-RDM-3
Ginna Records, Rev. 5
IP-SEP-2
Self Assessment, Rev. 4
IP-SEP-3
Ginna Station Management Observation, Coaching and Tours
Program, Rev. 2
S-16.13
RWST Water Makeup to Accumulators, Rev. 30
T-44.1
Condensate Test Tank for Standby AFW Pumps Filling or Draining,
Rev. 17
A-1603.0
Overview of the Ginna Station Work Control System, Revision 19
A-1603.1
Work Request / Trouble Report Initiation, Revision 14
A-1603.2
Work Order Initiation, Revision 15
A-1603.6
Post Maintenance / Modification Testing, Revision 8
A-1603.8
Work Order Processing for Emergency and/or After Hours
Maintenance, Revision 7
2.12
Inoperability of Equipment Important to a Safety, Revision 41
2.4
Control of Limiting Conditions for Operating Equipment, Revision 119
G-ORS-01
Screening Committee Guideline, Revision 50
IP-CAP-1.1
Operability and Past Operability Determination Checklist, Revision 2
IP-CAP-1.4
AR Extension Request, Revision 1
IP-CAP-1.8
Effectiveness Review Form, Revision 0
IP-CAP-2
Root Cause Analysis for Equipment Failures, Revision 4
IP-CAP-4
Problem Solving, Revision 1
IP-CAP-5
Event Trending Process, Revision 1
IP-CAP-6
10CFR021 Screening, Evaluating, and Reporting, Revision 2
IP-HPE-1
Human Performance Event Evaluation Process, Revision 3
IP-NPD-4
Nuclear Operations Group Work Prioritization, Revision 6
IP-PSH-1
Integrated Work Schedule, Revision 6
IP-PSH-2
Integrated Work Schedule Risk Management, Revision 6
OP-2.3.1
Draining & Operation at Reduced Inventory of the Reactor Coolant
System, Revision 71
SPG-02
Integrated Work Schedule Schedulers Handbook, Revision 11
(cont.)
of 6
Non-Cited Violations:
NCV 2001-06-01
Failure to Perform Flow Rate Determinations as per ODCM
NCV 2001-08-01
Failure to Include Acceptance Criteria in Procedures
NCV 2001-08-02
Failure to Implement MSIV Surveillance Requirement
NCV 2001-09-01
Inappropriate Procedures During Service Water Pump Motor
Replacement
NCV 2001-10-01
Failure to Identify Seismic Issue with Containment Isolation Valve
NCV 2002-02-01
RCS Make-up Flow Paths Were Inappropriately Isolated
NCV 2002-02-02
Improper Source Range Detector Calibration
NCV 2002-03-01
Failure to Control/Evaluate Compensatory Fire Protection Measure
NCV 2002-03-02
Unlocked Technical Specification High Radiation Area
NCV 2002-09-01
Failure to Utilize Mobile Loudspeakers for Transient Population
NCV 2001-09-02
Failure to Correct Equipment & Human Performance Problems
Quality Assurance Audits:
2000-0014-BKS
Corrective Action & Operating Experience Programs
2001-0004-DHK
Emergency Response Plan
2001-0009-JMT
Engineering and Configuration Control Audit
2001-0010-RTD
Problem Identification and Resolution Process Audit
2001-0013-TGT
Operations Audit
2001-0017-PJH
Audit of Ginna Station Technical Specifications
2002-0001-JMT
2002-0002-TGT
Maintenance Audit
2002-0003-BKS
Cooperative Management Assessment Program
2002-0004-RTD
Emergency Preparedness Audit
2002-0006-DHK
Radiation Protection Audit
Self-Assessments:
2001-0025
Corrective Action Process Effectiveness
2002-0023
Effectiveness of Corrective Actions for Areas for Improvement
Identified During January 2001 Self-Evaluation
2002-0031
Effectiveness Review of Contamination Control During Reactor
Cavity Decontamination
2002-0041
Quality Control Program Preparedness
2002-0042
Self-Assessment of NCV Related to Reduced Inventory
2002-0043
Self-Assessment of NCV Related to the Alert Notification System
(cont.)
of 6
Action Reports: (* Denotes CR generated as a result of this inspection; P denotes a Precursor Report)
1997-1447
2000-0188
2000-1176
2000-1268
2000-1301
2000-1489
2000-1630
2001-0001P
2001-0013P
2001-0131P
2001-0141P
2001-0326P
2001-0393P
2001-0457P
2001-0517P
2001-0676
2001-0740P
2001-0783
2001-0862
2001-0923
2001-1070P
2001-1148
2001-1325
2001-1341
2001-1365
2001-1395
2001-1465
2001-1632
2001-1691
2001-1702
2001-1749
2001-1757
2001-1764
2001-1767
2001-1774
2001-1802
2001-1840
2001-1867
2001-1879
2001-1888
2001-1921
2001-1921
2001-1943
2001-1969
2001-2091
2001-2131
2001-2140
2001-2227
2001-2245
2001-2245
2001-4355
2002-0038
2002-0070
2002-0101
2002-0109
2002-0126
2002-0127
2002-0142
2002-0150P
2002-0161
2002-0163
2002-0193
2002-0193
2002-0195
2002-0195
2002-0237P
2002-0244P
2002-0266
2002-0371
2002-0371
2002-0417
2002-0421
2002-0479
2002-0492
2002-0530
2002-0530
2002-0530
2002-0538
2002-0541
2002-0595P
2002-0661
2002-0670P
2002-0730P
2002-0756
2002-0766
2002-0821
2002-0822
2002-0878
2002-0904
2002-0931
2002-0948
2002-0976
2002-1014
2002-1022
2002-1028
2002-1028
2002-1146
2002-1146
2002-1149
2002-1151
2002-1151
2002-1170
2002-1202
2002-1362
2002-1508
2002-1564
2002-1593
2002-1596
2002-1634
2002-1663
2002-1753
2002-1759
2002-1770
2002-1809
2002-1849
2002-1941
2002-1997
2002-2035
2002-2035
2002-2060
2002-2097
2002-2116
2002-2260
2002-2261
2002-2271*
2002-2272*
2002-2273*
2002-2277
2002-2283*
2002-2286*
2002-2287*
2002-2288*
2002-2289*
2002-2290*
2002-2300*
2002-2303*
2002-2304*
2002-2308*
2002-2309*
2002-2311*
2002-2405
2002-2405*
2002-2411*
Work Orders:
WO-20103571 Repair Lug Crimps on the B Service Water Pump
WO-20103583 Repair Lug Crimps on the A, C, & D Service Water Pumps
WO-20200848 Trouble shoot and repair AOV-371, Indicates Mid-Position but 25%
Open (related to AR 2002-0756)
WO-20201827 Repair A Containment Sump Pump Level Switch (LS-2039)
WO-20202034 Operations Suspects That V-214 Leaks By
WO-20202266 Install PCR 2002-0027, Replace Emergency Siren System
WO-20202387 Reach Rod to V-214 Needs to Be Replaced
(cont.)
of 6
Miscellaneous Documents:
PORC Meeting Minutes for meetings 2001-0041; 2001-0042; 2001-0049; 2002-0004;
2002-0007; 2002-0014; 2002-0021; 2002-0024; 2002-0028; 2002-0035; 2002-0040;
2002-0042; 2002-0045; 2002-0048
Nuclear Safety Audit Review Board (NSRB) Minutes for meetings 243, 244, and 245
Modification PCR-2002-0012, Relocate the Siren Central Control Unit to Ginna
Modification PCR-2002-0027, Replace Emergency Siren System
Temporary Modification 2000-0007, A S/G Blow-down Corrosion Product Sampler,
Rev. 1
Temporary Modification 2001-0012, Temporary SI Accumulator Makeup Pump, Rev. 1
Updated Final Safety Analysis Report
5059SCRN-2002-0524, Replace Emergency Siren System (related to WO-20202266)
Maintenance Department Monthly Performance Indicator Report (i.e. - backlog),
September 2002
Nuclear Emergency Response Plan, Revision 20
ProActive Assessment of Workplace Factors (PAOWF), August 2002
(cont.)
of 6
D.
ADAMS Agencywide Documents Access and Management System
Air Operated Valve
Action Report
CFR
Code of Federal Regulations
Instruments & Controls
Non-Cited Violation
NRC
Nuclear Regulatory Commission
NSARB Nuclear Safety Audit Review Board
Offsite Dose Calculation Manual
PAOWF ProActive Assessment of Workplace Factors
Publicly Available Records System
Plant Change Request
Performance Indicator
Plant Operations Review Committee
Quality Assurance
Radiological Environmental Monitoring Program
RG&E
Rochester Gas and Electric Corporation
Reactor Water Storage Tank
Significance Determination Process
TM
TS
Technical Specification
Work Order