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#REDIRECT [[IR 05000325/2009003]]
{{Adams
| number = ML100360622
| issue date = 02/05/2010
| title = IR 05000325-09-003 & 05000324-09-003, on 07/30/09, Brunswick Steam Electric Plant
| author name = Musser R
| author affiliation = NRC/RGN-II/DRP/RPB4
| addressee name = Annacone M
| addressee affiliation = Carolina Power & Light Co
| docket = 05000324, 05000325
| license number = DPR-062, DPR-071
| contact person =
| case reference number = ML092110250
| document report number = IR-09-003
| document type = Inspection Report, Letter
| page count = 21
}}
 
{{IR-Nav| site = 05000324 | year = 2009 | report number = 003 }}
 
=Text=
{{#Wiki_filter:February 5, 2010
 
==SUBJECT:==
BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA
 
==Dear Mr. Annacone:==
On July 30, 2009, the US Nuclear Regulatory Commission (NRC) issued the subject inspection report for the Brunswick Steam Electric Plant, ADAMS accession ML092110250. In reviewing this report, it was noted that we inadvertently omitted the Selected Issue Follow-up Inspection in section 4OA2.3. Accordingly, we are providing a revised version of Inspection Report 05000325/324/2009003 that documents the above change.
 
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (The Public Electronic Reading Room).
 
I apologize for any inconvenience this error may have caused. If you have any questions, please contact me at (404) 562-4603.
 
Sincerely,
/RA/
 
Randall A. Musser, Chief Reactor Projects Branch 4 Division of Reactor Projects
 
Docket No.:
50-325, 50-324 License No.: DPR-71, DPR-62
 
Enclosure:
Inspection Report 05000325, 324/2009003
 
cc w\\encls:
See page 2
 
_________________________
 
XG SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRP
 
SIGNATURE GJW /RA/
JGW /RA/
RAM /RA/
 
NAME GWilson JWorosilo RMusser
 
DATE 02/05/2010 02/05/2010 02/05/2010
 
E-MAIL COPY?
YES NO YES NO YES NO YES NO YES NO YES NO YES NO
 
CP&L
 
cc w/encl:
R. J. Duncan, II Vice President Nuclear Operations Carolina Power & Light Company Electronic Mail Distribution
 
Director Site Operations Brunswick Steam Electric Plant Electronic Mail Distribution
 
Edward L. Wills, Jr.
 
Plant General Manager Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.
 
Electronic Mail Distribution
 
Christos Kamilaris, Director Fleet Support Services Carolina Power & Light Company Electronic Mail Distribution
 
Joseph W. Donahue, Vice President Nuclear Oversight Carolina Power and Light Company Electronic Mail Distribution
 
Brian C. McCabe Manager, Nuclear Regulatory Affairs Progress Energy Carolinas, Inc.
 
Electronic Mail Distribution
 
Phyllis N. Mentel Manager, Support Services Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.
 
Electronic Mail Distribution
 
Michael S. Williams, Manager, Training Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.
 
Electronic Mail Distribution
 
(Vacant)
Manager License Renewal Progress Energy Electronic Mail Distribution
 
Annette H. Pope Supervisor, Licensing/Regulatory Programs Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.
 
Electronic Mail Distribution
 
Senior Resident Inspector U.S. Nuclear Regulatory Commission Brunswick Steam Electric Plant U.S. NRC 8470 River Road, SE Southport, NC 28461
 
John H. O'Neill, Jr.
 
Shaw, Pittman, Potts & Trowbridge 2300 N. Street, NW Washington, DC 20037-1128
 
Peggy Force, Assistant Attorney General State of North Carolina P.O. Box 629 Raleigh, NC 27602
 
Chairman, North Carolina Utilities Commission Electronic Mail Distribution
 
Robert P. Gruber, Executive Director Public Staff - NCUC 4326 Mail Service Center Raleigh, NC 27699-4326
 
Brunswick County Board of Commissioners P.O. Box 249 Bolivia, NC 28422
 
James Ross, Nuclear Energy Institute Electronic Mail Distribution
 
Public Service Commission State of South Carolina P.O. Box 11649 Columbia, SC 29211
 
cc w/encl. (continued next page)
 
CP&L
 
cc w/encl. (continued)
W. Lee Cox, II, Section Chief Radiation Protection Section N.C. Department of Environmental Commerce & Natural Resources Electronic Mail Distribution
 
Warren Lee Emergency Management Director New Hanover County Department of Emergency Management 230 Government Center Drive Suite 115 Wilmington, NC 28403
 
CP&L
 
Letter to Michael from Randall A. Musser dated February 5, 2010
 
SUBJECT:
BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA
 
Distribution w/encl:
C. Evans, RII EICS L. Slack, RII EICS OE Mail RIDSNRRDIRS PUBLIC R. Pascarelli, NRR ((Regulatory Conferences Only))
RidsNrrPMBrunswick Resource
 
Enclosure with the PI data collected or transmitted for this indicator and none were identified.
 
Specific documents reviewed are described in the Appendix to this report.
* Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report.
 
b.
 
Findings No findings of significance were identified.
 
4OA2 Identification and Resolution of Problems
.1 Routine Review of Items Entered Into the Corrective Action Program a.
 
Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensees corrective action program. The review was accomplished by reviewing daily action request reports.
 
b.
 
Findings No findings of significance were identified.
 
.2 Semi-Annual Trend Review a.
 
Scope The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted.
 
Enclosure The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.
 
b.
 
Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:
* Improper loosening of RPV reference leg connection, NCR# 322354
*
Unit 2 interruption of Shutdown Cooling due to maintenance, NCR# 327475
*
Rx Hydro core spray check valve high pressure test jumper failure, NCR# 329677
*
Work accomplished with inadequate documentation, NCR# 330266
*
Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004
 
The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.
 
.3 Selected Issue Follow-up Inspection: 1B Fuel Pool Filter Leak
 
a.
 
Inspection Scope
 
The inspectors selected AR #335654, 1B Fuel Pool Filter Leak for detailed review. This AR was associated with a an entry into AOP 5.0, Radioactive Spills, High Radiation, and Airborne Radioactivity, due to a leak from the 1B fuel pool filter gasket. The inspectors reviewed this report to verify that the licensee identified the full extent of the issue, performed an appropriate evaluation, and specified and prioritized appropriate corrective actions. The inspectors evaluated the report against the requirements of the licensees corrective action program as delineated in corporate procedure CAP-NGGC-0200, Corrective Action Program, and 10 CFR 50, Appendix B.
 
b.
 
Findings
 
No findings of significance were identified.
 
4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
 
a.
 
Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee
 
Enclosure security procedures and regulatory requirements relating to nuclear plant security.
 
These observations took place during both normal and off-normal plant working hours.
 
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.
 
b.
 
Findings No findings of significance were identified.
 
4OA6 Management Meetings
.1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.
 
An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.
 
ATTACHMENT: SUPPLEMENTAL INFORMATION
 
Enclosure with the PI data collected or transmitted for this indicator and none were identified.
 
Specific documents reviewed are described in the Appendix to this report.
 
y Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report.
 
a.
 
Findings No findings of significance were identified.
 
4OA2 Identification and Resolution of Problems
.1 Routine Review of Items Entered Into the Corrective Action Program a.
 
Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensees corrective action program. The review was accomplished by reviewing daily action request reports.
 
b.
 
Findings No findings of significance were identified.
 
.2 Semi-Annual Trend Review a.
 
Scope The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted.
 
The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance
 
Enclosure reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.
 
b.
 
Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:
 
y Improper loosening of RPV reference leg connection, NCR# 322354 y
Unit 2 interruption of Shutdown Cooling due to maintenance, NCR# 327475 y
Rx Hydro core spray check valve high pressure test jumper failure, NCR#
329677 y
Work accomplished with inadequate documentation, NCR# 330266 y
Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004
 
The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.
 
4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities
 
a.
 
Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.
 
These observations took place during both normal and off-normal plant working hours.
 
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.
 
b.
 
Findings No findings of significance were identified.
 
4OA6 Management Meetings
.1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.
 
Enclosure An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.
 
ATTACHMENT: SUPPLEMENTAL INFORMATION
}}

Latest revision as of 06:43, 14 January 2025

IR 05000325-09-003 & 05000324-09-003, on 07/30/09, Brunswick Steam Electric Plant
ML100360622
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 02/05/2010
From: Randy Musser
NRC/RGN-II/DRP/RPB4
To: Annacone M
Carolina Power & Light Co
References
ML092110250 IR-09-003
Download: ML100360622 (21)


Text

February 5, 2010

SUBJECT:

BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA

Dear Mr. Annacone:

On July 30, 2009, the US Nuclear Regulatory Commission (NRC) issued the subject inspection report for the Brunswick Steam Electric Plant, ADAMS accession ML092110250. In reviewing this report, it was noted that we inadvertently omitted the Selected Issue Follow-up Inspection in section 4OA2.3. Accordingly, we are providing a revised version of Inspection Report 05000325/324/2009003 that documents the above change.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (The Public Electronic Reading Room).

I apologize for any inconvenience this error may have caused. If you have any questions, please contact me at (404) 562-4603.

Sincerely,

/RA/

Randall A. Musser, Chief Reactor Projects Branch 4 Division of Reactor Projects

Docket No.:

50-325, 50-324 License No.: DPR-71, DPR-62

Enclosure:

Inspection Report 05000325, 324/2009003

cc w\\encls:

See page 2

_________________________

XG SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRP

SIGNATURE GJW /RA/

JGW /RA/

RAM /RA/

NAME GWilson JWorosilo RMusser

DATE 02/05/2010 02/05/2010 02/05/2010

E-MAIL COPY?

YES NO YES NO YES NO YES NO YES NO YES NO YES NO

CP&L

cc w/encl:

R. J. Duncan, II Vice President Nuclear Operations Carolina Power & Light Company Electronic Mail Distribution

Director Site Operations Brunswick Steam Electric Plant Electronic Mail Distribution

Edward L. Wills, Jr.

Plant General Manager Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.

Electronic Mail Distribution

Christos Kamilaris, Director Fleet Support Services Carolina Power & Light Company Electronic Mail Distribution

Joseph W. Donahue, Vice President Nuclear Oversight Carolina Power and Light Company Electronic Mail Distribution

Brian C. McCabe Manager, Nuclear Regulatory Affairs Progress Energy Carolinas, Inc.

Electronic Mail Distribution

Phyllis N. Mentel Manager, Support Services Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.

Electronic Mail Distribution

Michael S. Williams, Manager, Training Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.

Electronic Mail Distribution

(Vacant)

Manager License Renewal Progress Energy Electronic Mail Distribution

Annette H. Pope Supervisor, Licensing/Regulatory Programs Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.

Electronic Mail Distribution

Senior Resident Inspector U.S. Nuclear Regulatory Commission Brunswick Steam Electric Plant U.S. NRC 8470 River Road, SE Southport, NC 28461

John H. O'Neill, Jr.

Shaw, Pittman, Potts & Trowbridge 2300 N. Street, NW Washington, DC 20037-1128

Peggy Force, Assistant Attorney General State of North Carolina P.O. Box 629 Raleigh, NC 27602

Chairman, North Carolina Utilities Commission Electronic Mail Distribution

Robert P. Gruber, Executive Director Public Staff - NCUC 4326 Mail Service Center Raleigh, NC 27699-4326

Brunswick County Board of Commissioners P.O. Box 249 Bolivia, NC 28422

James Ross, Nuclear Energy Institute Electronic Mail Distribution

Public Service Commission State of South Carolina P.O. Box 11649 Columbia, SC 29211

cc w/encl. (continued next page)

CP&L

cc w/encl. (continued)

W. Lee Cox, II, Section Chief Radiation Protection Section N.C. Department of Environmental Commerce & Natural Resources Electronic Mail Distribution

Warren Lee Emergency Management Director New Hanover County Department of Emergency Management 230 Government Center Drive Suite 115 Wilmington, NC 28403

CP&L

Letter to Michael from Randall A. Musser dated February 5, 2010

SUBJECT:

BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA

Distribution w/encl:

C. Evans, RII EICS L. Slack, RII EICS OE Mail RIDSNRRDIRS PUBLIC R. Pascarelli, NRR ((Regulatory Conferences Only))

RidsNrrPMBrunswick Resource

Enclosure with the PI data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the Appendix to this report.

  • Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report.

b.

Findings No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Items Entered Into the Corrective Action Program a.

Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensees corrective action program. The review was accomplished by reviewing daily action request reports.

b.

Findings No findings of significance were identified.

.2 Semi-Annual Trend Review a.

Scope The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted.

Enclosure The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.

b.

Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:

  • Improper loosening of RPV reference leg connection, NCR# 322354

Unit 2 interruption of Shutdown Cooling due to maintenance, NCR# 327475

Rx Hydro core spray check valve high pressure test jumper failure, NCR# 329677

Work accomplished with inadequate documentation, NCR# 330266

Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004

The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.

.3 Selected Issue Follow-up Inspection: 1B Fuel Pool Filter Leak

a.

Inspection Scope

The inspectors selected AR #335654, 1B Fuel Pool Filter Leak for detailed review. This AR was associated with a an entry into AOP 5.0, Radioactive Spills, High Radiation, and Airborne Radioactivity, due to a leak from the 1B fuel pool filter gasket. The inspectors reviewed this report to verify that the licensee identified the full extent of the issue, performed an appropriate evaluation, and specified and prioritized appropriate corrective actions. The inspectors evaluated the report against the requirements of the licensees corrective action program as delineated in corporate procedure CAP-NGGC-0200, Corrective Action Program, and 10 CFR 50, Appendix B.

b.

Findings

No findings of significance were identified.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a.

Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee

Enclosure security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.

b.

Findings No findings of significance were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.

An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure with the PI data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the Appendix to this report.

y Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report.

a.

Findings No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Items Entered Into the Corrective Action Program a.

Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensees corrective action program. The review was accomplished by reviewing daily action request reports.

b.

Findings No findings of significance were identified.

.2 Semi-Annual Trend Review a.

Scope The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted.

The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance

Enclosure reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.

b.

Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:

y Improper loosening of RPV reference leg connection, NCR# 322354 y

Unit 2 interruption of Shutdown Cooling due to maintenance, NCR# 327475 y

Rx Hydro core spray check valve high pressure test jumper failure, NCR#

329677 y

Work accomplished with inadequate documentation, NCR# 330266 y

Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004

The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a.

Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.

b.

Findings No findings of significance were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.

Enclosure An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.

ATTACHMENT: SUPPLEMENTAL INFORMATION