IR 05000443/2011010: Difference between revisions

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{{Adams
{{Adams
| number = ML12174A232
| number = ML120480066
| issue date = 01/20/2012
| issue date = 03/26/2012
| title = Draft Letter from C. Miller, Region I to P. Freeman, Site Vice President, North Region, NextEra Energy Seabrook, LLC, Seabrook Station - NRC Inspection Report 05000443-11-010
| title = IR 05000443-11-010; NextEra Energy Seabrook, LLC; 9/25/2011 - 12/2/2011 Seabrook Station (Problem Identification and Resolution; Follow-up to Operability and Plant Modifications)
| author name = Miller C G
| author name = Miller C
| author affiliation = NRC/RGN-I/DRS
| author affiliation = NRC/RGN-I/DRS
| addressee name = Freeman P
| addressee name = Freeman P
Line 10: Line 10:
| license number = NPF-086
| license number = NPF-086
| contact person =  
| contact person =  
| case reference number = FOIA/PA-2012-0119
| case reference number = G20120266, SECY-2012-0196
| document report number = IR-11-010
| document report number = IR-11-010
| document type = Inspection Report, Letter
| document type = Inspection Report, Letter
| page count = 23
| page count = 22
}}
}}


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=Text=
=Text=
{{#Wiki_filter:Inspector and Tech Reviewer Areas to focus on: 1. Cover letter messages and request 2. Executive Summary (ES) for appropriateness and need 3. Length of Open URI section 40A5.2 4. Summary of POD assumptions issues from TIA in ES and 40A5 5. What to address in plans is only in cover letter (management integration of inspector observations to TIA)6. No immediate safety concerns in ES only.7. List of ACRONYMS and Reference list ???????Mr. Paul Freeman Site Vice President, North Region Seabrook Nuclear Power Plant NextEra Energy Seabrook, LLC c/o Mr. Michael O'Keefe P.O. Box 300 Seabrook, NH 03874
{{#Wiki_filter:==SUBJECT:==
 
SEABROOK STATION - NRC INSPECTION REPORT 05000443/2011010 RELATED TO ALKALI-SILICA REACTION ISSUE IN SAFETY RELATED STRUCTURES
SUBJECT: SEABROOK STATION -NRC INSPECTION REPORT 05000443/2011010


==Dear Mr. Freeman:==
==Dear Mr. Freeman:==
On January 20, 2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Seabrook Station. The enclosed inspection report documents the inspection results, which were discussed on January 2 0 th with you and other members of your staff.The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
On January 20,2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Seabrook Station. The enclosed inspection report documents the inspection results, which were discussed at the exit meeting with you and other members of your staff.
 
The focus of this inspection was activities surrounding your development actions related to the Alkali-Silica Reaction (ASR) problem occurring in safety related structures and other structures of regulatory importance (covered by the maintenance rule). In particular, we reviewed your Prompt Operability Determinations for certain structures based on best available information.
 
At the beginning of the inspection report period, we noted some areas that still needed to be addressed based on available information and NextEra satisfactorily addressed them with revisions to the documents.
 
On January 20, 2011 a final exit meeting was conducted and lead by Mr. Richard J. Conte, Chief Engineering Branch No. 1 of my staff. During the meeting, my staff summarized the change in status of the new findings and our plans to issue a Task Interface Agreement between Region I and the Office of Nuclear Reactor Regulation simultaneously with this report.The TIA was placed in the public document room (ADAMS Accession No. MLXXXXXXX).
 
The purpose of the Task Interface Agreement was for the NRR staff to identify the review criteria in evaluating the operability determination for the "B" Electrical Tunnel affected by ASR (part of the Control Building)
in assistance to the Region I staff by addressing questions we had on the matter.Also on January 2 0 1h, we focused on and summarized observations on your plans with respect to the unwritten assumptions in your operability determinations.
 
The NRC staff noted that these I determinations listed no assumptions in the applicable sections and that the design basis code ACI 318-1971 was based on empirical data for determining certain parameters that were a part of the design bases. Also Poison's ratio on concrete cores were not being tested or evaluated and this ratio was in the UFSAR. The assumption of this empirical data was that the relationships were for ASR free concrete.


Specific areas for which your plans do not address unwritten assumptions being made in the prompt operability determinations were list in section 40A5.2 In consultation with our technical reviewers in headquarters and to address the current shortcomings on unwritten assumptions for your operability determinations, we have determine that your plans do not sufficiently provide information related to: 1) condition assessment (extent and characterization);
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.
2) cause of the ASR as it impacts current degradation and operability; 3) estimate of expansion to date and current expansion rate; 4) interim structural assessment as it impacts current operability vs. longer term structural assessment; and, longer term monitoring ensure operability in the near future vs. longer term of the duration of the license (1-2 years vs. longer); and, 5) short term mitigation or needed remedial actions. This is in distinction to your overall comprehensive plan for the problem.Accordingly, we request that you provide your plans to address the above issues within 30 days of the date of this inspection report. We noted that, from the exit meeting of January 2 0 th you have agreed to this request and to review the report in 15 days and let us know of your plans to honor our request or identify the need for a management meeting. We further request that, should a management meeting be needed on these issues, it should be conducted within 30 days of the date of this report and a final response time will be negotiated at the management meeting. If your root cause evaluation scheduled for Feb. 2012 and the associate corrective action plan for this significant condition adverse to quality addresses the above, please use them to respond to our request.Also, the report documents two NRC-identified findings of very low significance (Green) that were determined to involve a violation of NRC requirements.


Because of the very low safety significance, and because they are entered into your corrective action program, the NRC is treating these findings as Non-cited Violations, consistent with Section 2.3.2 of the NRC Enforcement Policy. If you contest any non-cited violations in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Seabrook Station. In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Resident Inspector at Seabrook. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of the NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.qov/readinq-rm/adams.html (the Public Electronic Reading Room).
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. In conjunction with the follow-up of two unresolved items, the focus of this inspection was a review of activities involving NextEra's analysis and evaluation related to addressing the Alkali-Silica Reaction (ASR) issue occurring in safety related and other important to safety concrete structures. As a part of this inspection, we reviewed your original and revised Prompt Operability Determinations (POD) for certain affected structures.


Sincerely,Christopher G. Miller, Director Division of Reactor Safety Docket No.: 50-443 License No.: NPF-86
During the exit meeting, Mr. Richard J. Conte, Chief Engineering Branch 1, summarized the findings and observations. In addition, he discussed NRC observations regarding your planned correCtive actions and assumptions being made in the NextEra operability determinations. The inspectors conctuded that these structures can currently perform their safety related functions despite the observed degradation due to ASR. However the NRC still has concerns associated with long term operability, therefore additional information is needed to determine: 1) how various characteristics of the concrete may be affected by ASR; 2) the related effects on other elements of the structures, such as rebar, due to groundwater in-leakage; and 3) the rate of progression of the ASR in structures at the site. lt is our understanding that these specific areas are being addressed in a comprehensive corrective action plan that was still being finalized by your organization at the end of the inspection.


===Enclosure:===
Therefore, we request that you summarize your plans to address the above issues at a management meeting to be conducted April 23, 2012, at NRC Headquarters in Rockville, MD.
Inspection Report No. 05000443/201110


===w/Attachment:===
At the meeting you should be prepared to focus on the following technical issues: 1) describe which applicable American Concrete Institute (ACl) 318 code relationships are affected by ASR and your plans to ensure the applicable licensing and design bases remain valid; 2) describe your comprehensive plans to understand the related effects and overall progression of ASR, its cause, and actions to correct and/or mitigate the issue; and, 3) provide a timeline for key actions, including those to address long term operability, how the degradation affects the design basis, and longer term management of the ASR issue. During the meeting we will discuss your overall corrective action plans, including the documents to be submitted to the NRC on the docket.
Supplemental Information cc w/encl: Distribution via ListServ In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.qov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,Christopher Miller, Director Division of Reactor Safety Docket No.: 50-443 License No.: NPF-86
Also, the report documents two NRC-identified findings of very low significance (Green) one of which involved a violation of NRC requirements, Because of the very low safety significance, and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations, consistent with Section 2.3.2 of the NRC Enforcement Policy. lf you contest any non-cited violations in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the RegionalAdministrator, Region l; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident lnspector at Seabrook Station. In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region l, and the NRC Resident Inspector at Seabrook.


===Enclosure:===
ln accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the NRC's
Inspection Report No. 05000443/201110
"Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of the NRC's document system, Agencyrvide Documents Access and Management System (ADAMS). The ADAMS is accessible from the NRC Web site at http:/lwww.nrc.govlreading-rmladams.html (the Public Electronic Reading Room).


===w/Attachment:===
Sincerely,
Supplemental Information cc w/encl: Distribution via ListServ Distribution w/encl: (via e-mail)W. Dean, RA D. Lew, DRA D. Roberts, DRP D. Ayres, DRP C. Miller, DRS P. Wilson, DRS A. Burritt, DRP L. Cline, DRP A. Turilin, DRP R. Montgomery, DRP W. Raymond, DRP, SRI J. Johnson, DRP, RI A. Cass, DRP, Resident OA M. Franke, RI, OEDO RidsNrrPMSeabrook Resource RidsNrrDorlLpll-2 Resource ROPreports Resource L. Pinkham, DRS R. Conte, DRS M. Modes, DRS SUNSI Review Complete: (Reviewer's Initials)DOCUMENT NAME: G:\DRS\Engineering Branch 1\-- MModes\20111213 050442_201110 Seabrook IP711158A ASR Follow UP.docx After declaring this document "An Official Agency Record" it will be released to the Public.To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy OFFICE RI/DRSI RI/DRS RI/DRP RI/DRS RI/DRS NAME SChaudhary MModes/ ABurritt/
,aA Christopher G. Miller, Director Division of Reactor Safety Docket No.: 50-443 License No.: NPF-86 Enclosure:
RConte/ CMiller/DATE 1/ /12 1/ /12 12/ /12 12/ /12 12/ /12 01FAIl-E9DCQ Docket No.: License No.: Report No.: Licensee: Facility: Location: Dates: Inspectors:
lnspection Report No. 050004431201 1010 w/Attachment: Supplemental Information cc w/encl: Distribution via ListServ
Accompanied by: Approved by: U.S. NUCLEAR REGULATORY COMMISSION REGION I 50-443 NPF-86 05000443/2011010 NextEra Energy Seabrook, LLC Seabrook Station Seabrook, NH 03874 September 25 -September 30, November 15-17, 2011 (Illinois)
November 28-29, 2011 January 20, 2012 (Conference Call)M. Modes, Senior Reactor Inspector, Region I S. Chaudhary, Reactor Inspector, Region I W. Raymond, Senior Resident Inspector, Seabrook Atif Shaikh, Reactor Inspector, Region III A. Sheikh, Senior Structural Engineer, NRR G. Thomas, Structural Engineer, NRR Richard J. Conte, Chief Engineering Branch 1 Division of Reactor Safety Enclosure


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000443/2011010; 9/25/2011
lR 0500044312011010;91251201 1 - 121212011; Seabrook Station (Problem ldentification and
-12/2/2011;
Seabrook Station (IP 7111115 and IP7111117).
 
This report covers an inspection by regional inspectors, and resident staff; with assistance from NRR structural specialists.
 
Two Green findings were identified.
 
The significance of most findings is indicated by their color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process".


The cross-cutting aspects for the findings were determined using IMC 0310, "Components Within Cross-Cutting Areas." Findings for which the Significance Determination Process does not apply may be Green, or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
Resolution; Follow-up to Operability and Plant Modifications).


===Cornerstone: Mitigating===
This report covers an inspection by regional inspectors and resident staff, with assistance from the Office of Nuclear Reactor Regulation (NRR) structural specialists. Two Green findings were identified. The significance of most findings is indicated by their color (Green, White, Yellow,
Red) using lnspection Manual Chapter (lMC) 0609, "Significance Determination Process" (SDP). The cross-cutting aspects for the findings were determined using IMC 0310,
"Components Within Cross-Cutting Areas." Findings for which the SDP does not apply may be Green, or be assigned a severity levelafter NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.


Systems
===Cornerstone: Mitigating Systems===
: '''Green.'''
: '''Green.'''
The inspectors identified a finding regarding NextEra's operability determinations for Category I structures with a reduced concrete modulus of elasticity caused by alkali-silica reaction in the concrete.
The inspectors identified a finding in that NextEra failed to fully evaluate potential structural and seismic response impacts in accordance with the requirements in NextEra procedure EN-AA-1001 after identifying a degraded and nonconforming condition related to degraded conditions for some safety related structures due to Alkali-Silica Reaction (ASR).


NextEra did not adequately evaluate with available information the effects of the reduced concrete modulus with respect to key aspects of structural design as described in the Updated Final Safety Analysis Report (UFSAR). Specifically, NextEra did not initially fully evaluate the effects of the reduced modulus on the dynamic response of Category I structures to seismic events relative to global response; the changes in the structural natural frequency; and, the effects on attached systems, components and anchors. Further, NextEra did not adequately evaluate the adequacy of shear capacity of electric tunnel concrete walls without shear reinforcement to resist lateral forces during seismic events.The failure to fully evaluate the degraded and nonconforming concrete modulus condition as required by procedure EN-AA-203-1 001 was a performance deficiency.
Specifically, the evaluation did not consider the following effects due to changed properties of concrete, is reflected in reduced values of the modulus of elasticity as measured directly from concrete core samples: 1) building natural frequency in the dynamic response; 2) performance of anchorages and embedment of systems and components attached to the structures; and, 3) shear strength or capacity of affected structures and the dynamic/flexural response especially those buildings without corresponding shear reinforcement'
The failure to conduct adequate prompt operability determinations per procedure EN-AA-203-1001 for degraded and nonconforming conditions associated with ASR was a performance deficiency relative to a self imposed standard. Specifically, the prompt operability determinations conducted following the identification of ASR in safety-related structures did not completely analyze the effects of the reduced modulus of elasticity on the dynamic and flexural response of the structures to seismic events for certain conditions. This performance deficiency was associated with the design control aspect of the Mitigating Systems cornerstone; and, based on a comparison to Example 3.i of Appendix E of IMC 0612, it was determined to be more than minor. Specificatty, the failure to conduct adequate operability determinations adversely affected the Mitigating Systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences because it required an additional evaluation to confirm that the design bases was met. The issue was evaluated using IMC 0609, "significance Determination Process," and was determined to be of very low safety significance (Green). Specifically, when evaluated under IMC 0609, Attachment 4, the performance deficiency was a design or qualification deficiency confirmed not to result in an actual loss of safety function. The finding had a cross cutting aspect in the area of problem identification and resolution, P.1(c), related to ensuring that issues potentially impacting nuclear safety are thoroughly evaluated. Specifically, NextEra did not fully evaluate conditions adverse to quality, including evaluating the effects of the reduced concrete modulus of elasticity for impact on operability of the affected structures. (Section 4OA5.1.c)


The performance deficiency was associated with the Mitigating Systems cornerstone and was determined to be more than minor based on a comparison with Appendix E.3.i of IMC 0612 because it adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events in order to prevent core damage. The issue was evaluated using IMC 0609, "Significance Determination Process" (SDP), and was determined to be of very low safety significance (Green). The finding had a cross cutting aspect in the area of problem identification and resolution, P.1(c), related to ensuring that issues potentially impacting nuclear safety are thoroughly evaluated.
Severitv Level lV. The inspectors identified a Severity Level lV non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR) 50.59(dX1), "Changes, Tests, and Experiments," because NextEra did not adequately evaluate a "use-as-is" determination, resulting in a defacto design change, for certain ASR impacted safety related structures.


Specifically, NextEra did not thoroughly evaluate conditions adverse to quality, including evaluating the effects of the reduced concrete modulus for impact on operability of the affected structures. (Section 1 R1 5)Severity Level IV. The inspectors identified a non-cited violation of 10 CFR 50.59(d)(1)because NextEra did not provide an evaluation that adequately documented why implementing a design change to address an identified reduction in the concrete modulus of elasticity for several Category I concrete structures, did not present a more than minimal increase in the likelihood of the occurrence of a malfunction of a structure, system, or component (SSC) important to safety previously evaluated in the UFSAR. Specifically, NextEra issued EC272057 on April 25, 2011, to address reduced concrete modulus of elasticity in the control building electric tunnel and the t containment enclosure building, but did not complete a 10 CFR 50.59 evaluation prior to implementing changes to the facility as described in the modification.
Specifically, NextEra did not complete a 10 CFR 50.59 evaluation, to ensure that the identified reduction in concrete modulus of elasticity did not present a more than minimal increase in the likelihood of the occurrence of a malfunction of a structure, system, or component (SSC)important to safety previously evaluated in the updated safety analysis report (USAR) prior to implementing changes to the facility as described in the engineering change EC272057 issued on April 25,2011.


The failure to evaluate changes to the facility as described in EC272057 was contrary to 10 CPR 50.59(d)(1)and was a performance deficiency warranting a significance evaluation in accordance with the NRC Enforcement Manual for Traditional Enforcement and Inspection Manual Chapter (IMC) 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Disposition Screening." The violation was determined to be more than minor in accordance with IMC 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Screening," because the inspector could not reasonably determine that the changes would not have ultimately required prior NRC approval.
The failure to evaluate changes to the facility as described in EC272057 was contrary to 10 CFR 50.59(dX1) and was a performance deficiency warranting a significance evaluation in accordance with the NRC Enforcement Manualfor Traditional Enforcement and IMC 0612,
"Power Reactor Inspection Reports," Appendix B, "lssue Disposition Screening." The violation was determined to be more than minor in accordance with IMC 0612, "Power Reactor Inspection Reports," Appendix B, "lssue Screening," because it could not reasonably be determined that the changes would not have ultimately required prior NRC approval. In accordance with Section 6.1.d.2 of the NRC Enforcement Policy, this violation is categorized as Severity Level lV because the resulting changes were evaluated by the SDP as having very low safety significance (Green), because it was a design or qualification deficiency confirmed not to result in an actual loss of safety function and because further evaluation determined that the structures remained operable despite the degraded modulus condition. The finding had a cross cutting aspect in the area of human performance - work practices, H.4(b), because NextEra personnel did not follow procedures. Specifically, NextEra personnel did not follow the requirements of Section 5.2.2 of the 5059 Resource Manual when preparing the 50.59 screen tor EC272057. (Section 4OA5.2.c)iii


The finding was evaluated using the SDP in accordance with IMC 0609,"Significance Determination Process," and determined to be potentially risk significant due to a design deficiency confirmed not to result in a loss of operability.
=REPORT DETAILS=


In accordance with Section 6.1.d.2 of the NRC Enforcement Policy, this violation is categorized as Severity Level IV because the resulting changes were evaluated by the SDP as having very low safety significance (Green). The finding had a cross cutting aspect in the area of human performance-work practices, H.4(b), because NextEra personnel did not follow procedures.
Backqround In June 2009, NextEra conducted walk downs of structures within the scope of license renewal as part of license renewal application preparations. ln June 2010, the License Renewal Application (LRA) was received by the agency. ln October 2010, the NRC staff noted that the licensee was beginning to formulate actions associated with both finalizing the operability determination for the control building (CB) and starting an extent of conditions review of other areas that may be subject to the alkali-silica reaction (ASR) degradation.


Specifically, NextEra personnel did not follow the requirements of Section 5.2.2 of the 5059 Resource Manual when preparing the 5059 screen for EC272057. (Section 1R17)Executive Summary The focus of this inspection was activities surrounding development actions related to the Alkali-Silica Reaction (ASR) problem occurring in safety related structures and other structures of regulatory importance (covered by the maintenance rule). In particular, NRC staff reviewed the Prompt Operability Determinations for certain structures based on best available information.
The ASR is a chemical reaction in concrete, which occurs over time in the presence of water, between the alkaline cement paste and reactive non-crystalline silica that is found in some common coarse aggregates. In the presence of water, the ASR for.ms a gel that expands, causing micro-craclis that change the physical structural propertiesl of the concrete, including compressive and tensile strength, modulus of elasticity, and Poisson Ratio. At Seabrook the below-grade concrete structures have experienced groundwater infiltration.


At the beginning of the inspection report period, we noted some areas that still needed to be addressed based on available information and these issues were satisfactorily addressed with revisions to the documents.
ln the summer of 2010, NextEra performed an lmmediate and Prompt Operability Determination (POD) for the CB "B" electrical tunnel structure based on core samples taken from the building, lnspection Report 05000443/2010004, issued November 1, 2010, documented the NRC review of the POD with no findings.


Prior NRC review of this area was documented in the following Inspection Reports 05000443/2010004, 2010005, 2011002, 2011003, and 2011007 and the results were summarized in the Background section of this report.One unresolved items was closed and sufficient information was obtained in order to determine the performance deficiency-50.59 screening to accept as-is conditions for reduced modulus of elasticity for certain safety related structures.
On May 12,2011, Inspection Report 05000443/2011002 identified two non-cited violations (NCV) of very low safety significance related to maintenance rule (Title 10 of the Code of Federal Regulations (10 CFR) 50.65 a(1) and b(2)) monitoring of structures. One of the NCVs related NextEra's failure to properly monitor the structural performance of the CB resulting in degraded conditions - 10 CFR 50.65 (aX1) (NCV 2011-002-01). Also in May 2011, License Renewal Inspection Report 05000443/2011007 (1P71002) reflected an overall inspection result as follows: "Except for Structures Monitoring Program, results support a reasonable assurance determination for license renewal." The structure monitoring program had not addressed the ASR condition.


Another unresolved item was left open -Prompt Operability Determinations for certain safety related structure with the ASR problem. Another finding of very low safety significance was determined in the course of the operability determination review. Both findings were summarized above.The inspectors observed that NextEra plans for the ASR problem were not addressing unwritten assumptions in the operability determinations.
On August 12, 2011, lnspection Report 05000443/2011003, identified a NCV of very low safety significance related to the untimely operability determinations regarding the extent of condition review for other buildings affected by ASR. The report also identified two unresolved items (URl) related to the operability determinations. Specifically the report identified: 1) the need for additional information related to open operability determinations, one for the CB "8" electrical tunnel, and the other operability determinations for the extent of conditions review for five other areas/structures with evidence of ASR (URl 201 1-003-03); and,2) potential inadequate screening in accordance with 10 CFR 50.59 for accepting the reduced values found on compressive strength and modulus of elasticity for the "B" Electrical Tunnel and the Containment Enclosure Building (URl 201 1-003-02).


These operability determinations listed no assumptions in the applicable sections.
1 Material properties defined in the supplemental section of this report ln September 2011, Region I obtained assistance from the Office of Nuclear Reactor Regulation (NRR) through a Task Interface Agreement (TlA) in order to assist in the review of the open PODs.


The design basis code ACI 318-1971 was based on empirical data for determining certain parameters that were a part of the design bases.Poisson's ratio on concrete cores were not being tested or evaluated and this ratio was in the UFSAR. The assumption of this empirical data was that the relationships were for ASR free concrete.
==OTHER ACTIVITIES==
4OI2 Problem ldentification and Resolution (71152-1 sample)
Annual Sample: Corrective Actions Associated with Alkali-Silica Reaction in Safetv Related Structures Inspection Scope This review was to assess progress in the development of a corrective plan and implementing schedule to address the ASR degradation issue including: initial assessments of all buildings potentially affected by the problem; root or apparent cause of the problem; control of in-situ testing such as crack mappingiindexing; control of contractor testing and laboratory test facilities in accordance with quality assurance requirements; and any mitigation or long term monitoring actions. The inspectors reviewed laboratory testing to address the ASR degradation with specific focus on the CB ("8" Electrical Tunnel). Laboratory testing was observed during the week of November 14,2011, to ensure proper sample controls, test preparation, and conduct of the test.


Specific areas for which the plans do not address unwritten assumptions being made in the prompt operability determinations were list in section 40A5.2
During the week of November 28,2011, the inspectors reviewed historical documentation from the construction phase of the plant, correlations between the concrete strength value determined by the recent core samples, and the original strength values determined at the time of concrete placement. The licensee's projected plan and schedule for further studies and assessment of the ASR problem were discussed and reviewed with cognizant engineering and management personnel. lnspectors also reviewed the licensee's control of contractors and laboratory facilities used to analyze concrete core samples. The inspectors reviewed the licensee's procedures for administration and control of engineering and testing service vendors and contactors.


To address the above and in conjunction with the NRR technical reviewers, the inspectors noted that the current plans were not finalized and what was existing did not specifically address the unwritten assumptions in the following areas: 1) condition assessment (extent and characterization);
Additionally, the inspector reviewed the results and documentation of American Society of Mechanical Engineers (ASME) Code Section IWL inspection of the containment.
2) cause of the ASR as it impacts current degradation and operability; 3)estimate of expansion to date and current expansion rate; 4) interim structural assessment as it impacts current operability vs. longer term structural assessment; and, longer term monitoring ensure operability in the near future vs. longer term of the duration of the license (1-2 years vs.longer); and, 5) short term mitigation or needed remedial actions.The NRC staff summarized why there is no immediate safety concerns for the existing conditions:
walkdowns confirm no significant degradation, no visual evidence of distortion nor visible evidence of rebar corrosion; overall evidence of sufficient stiffness remaining;
No appreciable evidence of cracking where found, in isolated sections of the wall; degradation appears to be localized;
We know from best available research that the ASR rate slowly progresses and there is some evidence that it has progressed to a plateau but it needs to be confirmed by testing; parameters obtained for compressive strength and modulus of elasticity indicate robust design to strength of the concrete poured (4K psi concrete used in buildings only needing 3K psi concrete and no significant negative shift on seismic analysis.On January 20, 2011 a final exit meeting was conducted.


During the meeting, NRC staff summarized the change in status of the new findings and plans to issue a Task Interface Agreement between Region I and the Office of Nuclear Reactor Regulation simultaneously with this report. The TIA was placed in the public document room (ADAMS Accession No.MLXXXXXXX).
Findinqs and Observations No findings were identified. The inspector noted that a comprehensive corrective action was still under development. NextEra classified this issue as a significant condition adverse to quality and was in the progress of completing a root cause analysis, which was scheduled to be completed in February 2012 in order to support an Engineering Evaluation in March 2012. The inspectors noted that NextEra's plans to date did not address some key issues related to ASR that include but are not limited to:
a.


The purpose of the Task Interface Agreement was for the NRR staff to identify the review criteria in evaluating the operability determination for the "B" Electrical Tunnel affected by ASTR (part of the Control Building)in assistance to the Region I staff by addressing questions related to the problem.Enclosure 2
b.
: (1) Need for other concrete core testing (i.e., low stress range stiffness damage tests) to assess expansion-to-date or severity of degradation in the critical direction of the thickness with no rebar ties and lesser resistance to expansion; Basis for the representativeness of concrete core sampling in the buildings for those taken to date and those to be taken, should they occur; lmpact of core boring and re-grouting on the building structural integrity; and Potential effects of other degradation mechanisms from an "aggressive" groundwater environment along with the presence of ASR.


=REPORT DETAILS=
Methods Used in Evaluatinq Structural Inteqritv The NRC staff noted that the methods used in evaluating structural integrity for the selected buildings were based on the correct design basis code ACI 318-1971.
Background In June 2009, NextEra conducted walkdowns of structures within the scope of license renewal as part of license renewal application preparations.


In June, 2010 the License Renewal Application (LRA) was received by the agency. In October 2010, the License Renewal Audit results noted the alkali-silica reaction (ASR) problem and pointed to need for a good number of requests for additional information in this area since the issue was newly discovered for the site (noted as a area to address in the GALL, Generic Aging Lessons Learned, Revision 1). In the Fall of 2010, NextEra performed an Immediate and Prompt Operability Review (POD) based on core samples taken in Control Building in August 2010. In November 2010, Inspection Report 05000443/2010004 and, in February 2011, Inspection Report 2010005, followed developments in this area from an operability viewpoint.
However, the mathematical relationships in this code were based on empiricaldata, from testing of non-degraded concrete, for determining key ratios that are a part of the design bases and used for determining tensile and shear strength or capacity in addition to compressive strength. These strength values were important in the building loading analysis during normal or upset conditions such as for seismic events. More importantly, while some testing for the modulus of elasticity was done, it was not clear if the plans would result in additional testing of concrete cores for this parameter or any independent testing associated with other key design parameters such as Poisson's Ratio, shear modulus, or bulk modulus. With these parameters known, various strengths or capacities can be determined such as for tensile and shear strength. In addition, the plans that the inspectors reviewed did not address variation in mechanical properties of the concrete in different directions due to ASR cracking nor the effect of the ASR expansion on stresses in the rebar. These parameters were important in order to ensure that the current licensing and design basis was maintained. The licensee representatives agreed to address the assumptions or establish relationships for the current conditions at Seabrook. Accordingly this area is unresolved pending completion of license actions as noted above and further NRC staff review (URf 05000 4/.312011 01 0-01, Corrective Actions Associated with calculation methods used to address the ASR lssue)
Control of ContractorsA/endors and Laboratorv Testinq The reviewers noted that NextEra had engaged knowledgeable vendors, appropriate consultants, and experts for testing, analysis, and evaluation of the effects of ASR on the serviceability and safety of the affected structures. Also, during the week of November 14,2011, a Region lll inspectorreviewed laboratorytestingforcompressive strength on 15 concrete core samples taken from the CB "8" electricaltunnel in the October 2011 time frame. This testing was being completed to resolve discrepant information for compressive strength testing between two different contractors.


In these reports, no findings were noted since laboratory results determined compressive strength and modulus of elasticity met UFSAR values (degradation into reserve strength not design margin). In May 2011, Inspection Report 05000443/2011002 identified two noncited violations of very low safety significance in the structures monitoring area with respect to the maintenance rule (10 CFR 50.65 a(1 ) and b(2)).Also in May 2011, License Renewal Inspection (IP71002)
The testing was conducted at a laboratory in Northbrook, lllinois. All 15 core samples were compression tested. Photographs were taken for all core samples prior to loading for compression test and after fracture. Three cores had small length samples cut from them to be used by Seabrook for further petrography. Sample preparation (capping)was done in accordance with American Society for Testing and Materials (ASTM) C617.
Report 05000443/2011007 had an overall result: "Except for Structures Monitoring Program, results support a reasonable assurance determination for license renewal." As the year progressed, NextEra continued to identify and characterize the below-grade structures at Seabrook having experienced groundwater infiltration and a resultant reduction in concrete material properties.


NextEra determined the degraded concrete condition was most likely due to distress from ASR in the concrete.
(2)
(s)
: (4) 40A5 Compression testing was done in accordance with ASTM C39. With respect to laboratory conditions for testing of concrete cores, the inspector verified: 1) organized and clean working area during both sample preparation (measurements and cutting)and compression testing; 2) adequate lighting available at all times; 3) ambient room temperature (- 68"F) observed during preparation and testing; and 4) core samples were adequately stored and labeled in individual bags.


ASR is a chemical reaction in concrete over time between the alkaline cement paste and reactive non-crystalline silica which is found in common coarse aggregates.
The inspector observed the care taken to ensure only one core was handled at any given time so as not to confuse cores during measurements, cutting, and testing. With respect to equipment calibration, the inspector verified proper equipment documentation and calibration. With respect to test technician qualifications, the inspector also verified qualification records. The inspector also reviewed the Altran Commercial Grade Dedication Plan.


The reaction only occurs in the presence of water and forms a gel that expands, forming micro-cracks that change the strength of concrete system. NextEra is in the discovery phase of condition assessment along with extent of condition reviews in order to support other building operability determinations and a plan to conduct an engineering evaluation which would appear to constitute a long term operability review (40 year license term) along with mitigation and monitoring measures.The appearance of ASR degradation in safety related concrete structures was the first noted in the nuclear industry in the United States and could be significant related to preservation of reserve capacity with building design loads as reflected in the current licensing basis during normal operations and aging management over the period of extended plant operation.
No concerns were noted with respect to quality control during all aspects of compression testing. All 15 destroyed cores were shipped back to Seabrook including the cut samples to be used for petrography. These results were to be evaluated by NextEra.


While the problem was noted as an aging effect in a license renewal topical report, the appearance of ASR reflected a newly discovered aging effect at Seabrook that needs to be managed for license renewal.In August 2011, Inspection Report 05000443/2011003 addressed a noncited violation of very low safety significance related to the untimely Initial and Prompt ODs for results on extent of condition review for other buildings affected by ASR. Two unresolved items was also opened, one dealing with a potential inadequate screen in accordance with 10 CFR 50.59 for accepting the reduce parameter found on compressive strength and modulus of elasticity for the "B" Electrical Tunnel and the Containment Building.
Other Activities (Open) Unresolved ltem 05000443/2011003-03. Open Operabilitv Determinations for Safetv-Related Stru ctu res Affected bv Al kal i-Sil ica Reaction Insoection Scope The NRC staff reviewed NextEra actions to develop finalized operability determinations along with the review for extent of conditions. The review included the open aspects as documented in the originating inspection report for which NextEra was to provide additional information related to: 1) effect of the reduced modulus of elasticity on natural frequency of the structures (applied to CB - "8" Electrical tunnel and other structures being evaluated in the extent of conditions review such as for the Containment Building (CEB); 2) the effect of the modulus of elasticity on structure flexural response as related to components attached to the structures, such as pipe and cable trays supports and their anchor bolts; 3) related effects from increased flexure of building on the loading and seismic effects on safety related pipes and cable tray supports; and, 4) effect of reduced parameters on the whole building (global) response of the CEB structure to seismic loads including further information of the effect on stress and strain in the concrete and rebar system. With respect to numbers 1 and 2 above, the inspectors reviewed the operability determinations for the below listed safety related structures degraded by ASR. The inspectors verified the basis for why the Radiological Control Area tunnel was confirmed to not be affected by ASR. The inspectors reviewed operability determinations for the following buildings:


The other unresolved dealt with the open prompt operability determinations associated with the "B" Electrical Tunnel and the Enclosure 3 building subjected to an extent of conditions review. In August of 2011 a Task Interface Agreement (TIA) was issued between Region I and the Office of Nuclear Reactor Regulation on the ASR issue. The response to the TIA is publicly available (ADAMS Accession No.MLxxxxxxxxx).
===.1 a.===
. Control Building - "8" Electrical Tunnel, o Containment Enclosure Building,
. Diesel Generator Fuel OilTank Rooms,
. Residual Heat Removal Equipment Vaults, and r Emergency Feedwater Pump House.


The purpose of this inspection was to followup on the unresolved items and to work with the NRR technical reviewers in developing the answers to the questions posed in the TIA.1.
The inspectors utilized site records and interviews to determine the design basis for the safety related structures in addition to those summarized in Sections 3.7 and 3.8 of the Updated Final Safety Analysis Report (UFSAR).


==REACTOR SAFETY==
b. Observations For the open aspects of numbers 1 and 2 above, a finding was identified and addressed in Section 4OA5.1.c. This section also noted a new issue identified by NRC staff related to shear reinforcement for the walls of the CB and the diesel generator building.
Cornerstones:
Initiating Events, Mitigating Systems, and Barrier Integrity 1 R15 Operability Determinations and Functionality Assessments (71111.15
-0 samples)a. Inspection Scope As a part of the review of an unresolved item (see section 4OA5.2), the inspectors, in conjunction with technical reviewers from the Office of Nuclear Reactor Regulation, reviewed the adequacy of operability determinations for the below grade concrete walls of seismic Category I buildings affected by alkali-silica reaction.


The review focused on the specific design for the buildings affected by an alkali silica reaction and operability was addressed by two prompt operability determinations, one, to address the control building and the other to address the following extent of conditions with five other building/structures:
The open aspects of numbers 3 and 4 were updated but not completely resolved due to the need to obtain additional information. At the beginning of the inspection, the NRC staff review determined that the initial evaluation for the CEB did not address the open aspects of numbers 1 and 2 above; and, in particular, the response of the entire structure (whole building) to seismic loading comparable to the methods described in UFSAR 3.8. This included how the induced seismic stresses would shift between the concrete and the steel in adjoining sections of the structure. In response, NextEra noted that these issues would be factored into the analytical model (finite element analysis) to reanalyze the CEB using the as-measured worst case elastic modulus applied to ASR-lm pacted sections.
Containment Building, Emergency Diesel Generator Buildings (fuel oil rooms), Residual Heat Removal Equipment Vaults, Emergency Feedwater Pump House, and the Radiological Control Access (RCA) tunnel.b. Findings Inadequate Operability Determinations


=====Introduction.=====
Revision 1 of the applicable operability determination for the CEB provided additional quantitative and qualitative analysis, for the available information, which addressed groundwater intrusion limited to less than 25 percent of the perimeter of the below grade portion of the building; the effect of the reduced modulus on the natural frequency; and the effect on shear capacity that indicated that the dynamic and flexural response had a minimaleffect.
In April 2011, NextEra identified a degraded and nonconforming condition related to reduced modulus of elasticity for buildings housing safety related equipment, but did not thoroughly evaluate potential impacts in accordance with the requirements in NextEra procedure EN-AA-203.
 
Specifically, the evaluation did not consider the affect of the reduced modulus on: overall stiffness and resulting seismic response, concrete material property changes affecting natural frequency and therefore the amplitude of the seismic response, and the performance of systems and components attached to the affected structures during seismic events.Description.
 
In April 2011 NextEra determined that certain below grade concrete walls were affected by alkali-silica reaction (ASR). The analysis of concrete cores showed a reduced concrete modulus of elasticity in the control building / electric tunnel (AR581434), containment enclosure building (AR1644074)and three other seismic Category I buildings (AR1664399).


The lowest measured modulus was about 40% less than the design value of 3.62E+03 ksi.NextEra completed prompt operability determinations for the affected Category I concrete structures (reference ARs 581434, 1644074 and 1664399) as required by NextEra Procedure EN-AA-203-1001, "Operability Determinations/Functional 4 Assessments." In accordance with the procedure EN-AA-203-1001, a POD must include: identification of current licensing basis functions and performance requirements as listed in the UFSAR; identification of the minimum design basis values necessary to satisfy the SSC design basis safety functions; and evaluation of the effects of the degraded condition on the ability of the SSC to meet its specified function and performance requirements.
In conclusion, this area remained open pending further developments and completion of licensee actions as noted above and further NRC staff review. While this unresolved item remains open, the NRC staff determined that the affected safety-related structures can currently perform their safety functions. This conclusion was based on the following:
. Conservative safety load factors in controlling load conditions and engineering conservatisms in design provide reasonable expectation that affected structures can perform their safety function, despite the current licensing basis design margin being reduced by the change of mechanical properties;
. Field walk-downs confirm no visible indication of significant deformation, distortion, or displacement of structures, or rebar corrosion;
. Evidence of ASR limited to localized areas in the concrete walls; and
. Progression of ASR degradation occurs slowly based on existing operating experience and published literature, and the licensee continues to monitor.


During the week of September 28, 2011, the inspectors in conjunction with technical reviewers from the Office of Nuclear Reactor Regulation reviewed NextEra's competed PODs for the ASR-affected Category I concrete structures.
This unresolved item related to operability of ASR affected safety related buildings remained open for NextEra to evaluate ASR effect on cable and pipe loadings (number 3) and evaluate ASR effect on the CEB whole building response (number 4).


It was determined that the evaluations were not complete with respect to available information since NextEra did not evaluate the degraded condition with respect to key aspects of the structure design as described in UFSAR. Specifically, the initial PODs did not adequately address the effects of the reduced modulus of elasticity in the following areas: 1. As a result of further review of the design bases, the NRC staff determined that the walls below grade in the Control Building 'B' Electrical Tunnel do not contain shear reinforcement to resist dynamic lateral forces acting on the wall during a design basis earthquake.
c. Findinq Related to Operabilitv Determinations and Functionalitv Assessments -
Inadequate Operabilitv Determinations lntroduction. The inspector identified a finding in that NextEra failed to fully evaluate potential structural and seismic response impacts in accordance with the requirements in NextEra Procedure EN-AA-1001 after identifying degraded and nonconforming condition related to reduced concrete modulus of elasticity due to ASR degradation for safety related structures. The evaluation did not consider the following effects due to changed properties of concrete as measured directly from building concrete core samples:
building natural frequency in the dynamic response; performance of anchorages and embedment of systems and components attached to the structures; and shear strength or capacity of affected structures and the dynamic/flexural response especially for those building walls without corresponding shear reinforcement.


The design of the wall intentionally depends on the strength of the concrete alone to resist these dynamic forces and this information was not evaluated for the degraded conditions.
=====Description.=====
NextEra analysis of concrete cores samples taken following the April 2011 determination that certain below grade concrete walls in safety related structures were affected by ASR, indicated a reduced modulus of elasticity and compressive strength.


The same was true for the Diesel Generator Building.The modulus of elasticity of concrete was a function of concrete compressive strength which is generally higher in the as-cast condition than assumed in the design. The concrete used in construction of Seabrook structures was formulated to have a design strength greater than 3000 psi. However, as stated in the Seabrook Updated Final Safety Analysis Report, Revision 12, Section 3.8, "While variability in concrete modulus has no significant effect on structural design, it influences structural stiffness and natural frequency, and, subsequently, the amplified response spectra of the seismic analysis." 2. Changes in the modulus of elasticity affect the material concrete properties and, therefore, the natural frequency of the structure, which affects how the buildings are analyzed in the seismic analysis.
Although the compressive strength reduction was viewed by NextEra as slight and acceptable, the lowest measured modulus was about 40 percent less than the design value of 3,620 kpsi.


NRC reviews determined that the prompt operability determinations addressed the dynamic response of the structures in a qualitative manner noting that the ASR impacted walls are below grade and the structural loadings would be governed by the ground response spectra assumed in the original design. The initial evaluations did not sufficiently address the impact of the reduced modulus on the structure natural frequencies in a quantitative manner to validate that the structure response would remain rigid or that there would be a amplification of the response.
NextEra completed operability determinations for certain affected safety-related concrete structures as required by NextEra Procedure EN-AA-203-1001, "Operability DeterminationsiFunctional Assessments." ln accordance with the Procedure EN-AA-203-1001, an operability determination must include: identification of current licensing basis functions and performance requirements as listed in the UFSAR; identification of the minimum design basis values necessary to satisfy the structure, system, or component (SSC) design basis safety functions; and evaluation of the effects of the degraded condition on the ability of the SSCs to meet its specified function and performance requirements.


Specifically, the initial evaluation did not verify there.would be no amplification of the motions beyond those in a ground response spectra as assumed in the seismic analysis per UFSAR 3.7(B).2.3. The initial POD addressed the effects of the reduced modulus on components housed within the structures, such as pipe supports, cable trays and component support anchors. NRC review determined that the initial evaluations addressed the impacts on the internal components in a qualitative manner, but did not verify the equipment performance would remain bounded by the analysis in the original design as described in UFSAR 3.7 and 3.8. Specifically, the initial evaluation did not verify Enclosure IL 5 there would be no amplification of the motions beyond those in a ground response spectra as assumed in the seismic analysis per UFSAR 3.7.(B).2.
During the week of September 26,2011, NRC staff determined that the completed operability determinations were not sufficient in that they did not address the impact of the degraded condition on key aspects of the structure design as described in UFSAR.


Further, the initial evaluation did not evaluate the potential impacts on anchor or wall shear capacities caused by ASR induced changes in material properties beyond that allowed for as described in UFSAR 3.8.In response to the NRC-identified issues, NextEra completed' additional evaluations that determined the structures and other affected systems and components remained functional for design basis conditions.
Specifically, NextEra failed to address the ASR induced effects of the reduced modulus of elasticity on seismic dynamic and flexural response in the following areas:
r Building naturalfrequency in the dynamic response;
. Performance of anchorages and embedment of systems and components attached to the structures affected by ASR; and
. Shear capacity of affected walls especially for those buildings without corresponding shear reinforcement such as for the CB and the emergency diesel generator building.


On October 14, 2011, NextEra completed Calculation C-S-1-10163, and revisions to the PODs for AR581434 (CB/ ET) and AR1664399 (CEB and other Category I Structures).
NextEra performed additional reviews and updated the operability determinations for the affected areas in response to these concerns, on October 14,2011. The licensee determined that the structures and other affected systems and components remained functional for design basis conditions but were degraded.


The NRC determined that NextEra's additional analysis and revisions to the PODs adequately addressed the concerns discussed above. Specifically, the analysis confirmed a minor impact on the overall response of the structure during a seismic event, a small effect on the structure's natural frequencies that results in no appreciable amplification of the ground response during a seismic event, and no impact on the ability of the equipment anchors to perform their function due to the quality of the concrete and construction methods used.Analysis.
The NRC reviewed the updated operability determinations and associated calculations determining that the additional areas needing evaluation were addressed and that the structures remained "operable but degraded." The previous determination indicated that the evaluated structures were "operable." Specifically, NextEra used quantitative and qualitative information with respect to the degraded concrete conditions as noted below.


The inspectors determined that not following a self imposed standard, not completely analyzing the effects of the reduced modulus of elasticity on Category I structures based on available information, per procedure EN-AA-203-1001 was a performance deficiency.
With respect to dynamic response and the change in the natural frequency of the structures, licensee's additional evaluation determined that the shift in naturalfrequency was minimal and remained well above the ground response peak frequency range such that the response of the structures remained rigid. With respect to the ability of the equipment anchors and embedment to perform their function, the licensee's additional evaluation noted that there was no appreciable impact. The licensee also determined that the impact on the flexural capacity of seismic buildings with respect to shear stress was minimal, and the resultant stresses on the steel and concrete remained below the design stress limits with margin.


Specifically, because the reduced modulus affected the dynamic response of Category I structures to seismic events relative to global response, changes in natural frequency and the effects on attached systems and components, procedure EN-AA-203-1 001 required that these impacts be evaluated as part of the prompt operability determination.
Following review, the inspector determined there was a reasonable expectation that the structural integrity remained intact under design loads, and the buildings remained operable but degraded. NextEra continued to review the degraded concrete issue within the corrective action program, including the effects on the long term reliability of the structures.


This performance deficiency was associated with the Mitigating Systems cornerstone and was determined to be more than minor because, based on a comparison with Examples 3.i of Appendix E of IMC 0612, it adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events in order to prevent core damage. Specifically, the effects of the reduced modulus of elasticity on the dynamic response of Category I structures to seismic loading required further evaluation to demonstrate the structures and enclosed systems remained functional as described in the licensing and design bases. The issue was evaluated using IMC 0609, "Significance Determination Process" (SDP), and was determined to be of very low safety significance (Green). Specifically, when evaluated under IMC 0609, Attachment 4, the performance deficiency was not a design or qualification deficiency resulting in an actual loss of safety function, was not a loss of a barrier function, and was not potentially risk significant for external events. The finding had a cross cutting aspect in the area of problem identification and resolution, P.1(c), related to ensuring that issues potentially impacting nuclear safety are thoroughly evaluated.
Analvsis. The inspectors determined that NextEra's failure to conduct adequate prompt operability determinations per Procedure EN-M-203-1001 for degraded and nonconforming conditions associated with ASR was a performance deficiency relative to a self imposed standard. Specifically, the operability determinations conducted following identification of ASR in safety-related structures did not completely analyze the effects of the reduced modulus on the dynamic and flexural response of safety related structures to seismic events along with the effect on attached systems and components. This performance deficiency was associated with the design control aspect of the Mitigating Systems cornerstone; and, based on a comparison to Example 3.i of Appendix E of IMC 0612, it was determined to be more than minor. The issue was evaluated using IMC 0609, "significance Determination Process," and was determined to be of very low safety significance (Green). The finding had a cross cutting aspect in the area of problem identification and resolution, P.1(c), related to ensuring that issues potentially impacting nuclear safety are thoroughly evaluated. NextEra did not thoroughly evaluate conditions adverse to quality, including evaluating the effects of the reduced concrete modulus for impact on operability of the affected structures.


Specifically, NextEra did not thoroughly evaluate conditions adverse to quality, including evaluating the effects of the reduced concrete modulus for impact on operability of the affected structures.
===.2


=====Enforcement.=====
=====Enforcement.=====
Because this finding does not involve a violation and has very low safety significance, it is identified as FIN 05000443/2011-10-01, Incomplete Operability Determination for Degraded Concrete Structures Housing Safety-Related Equipment based on available information.
Because this finding does not involve a violation and has very low safety===
significance, it is identified as FIN 05000443/2011-10-02, lncomplete Operability Determ i nation for Degraded Concrete Stru ctu res Hous i n g Safety-Re lated Equipment.


6 1R17 Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications (71111.17-0 sample)a. Inspection Scope As a part of the review of an unresolved item (see section 40A5.1), the inspector reviewed EC272057, dated April 25, 2011, for adequacy in which the EC was a design change to address reduced concrete modulus of elasticity in the control building electric tunnel and the containment enclosure building.
(Closed) Unresolved ltem 05000443/201 1003-02. 50.59 Evaluation for Acceptinq Reduced Modulus of Elasticitv in Certain Safetv-Related Structures Affected bv Alkali-Silica Reaction Inspection Scope As part of the review of this unresolved item, the inspectors continued to review EC272057, dated April 25, 2011, for adequacy in which the engineering change (EC)was a design change to address reduced concrete modulus of elasticity in the CB electric tunnel and the containment enclosure building. The review was to determine if only a 10 CFR 50.59 screening was adequate to accept "as-is" conditions for this concrete material property. The inspector reviewed NextEra's revocation of this EC, Observations This issue was closed based on the revocation of the EC, and on the Severity Level lV NCV, as noted below.


The review was to determine if only a 50.59 screening was acceptable to accept "as-is" conditions for this concrete material property which was degraded from the design bases as reflected in the UFSAR apparently due to the ASR problem.b. Finding Inadequate 50.59 Screen Evaluation for EC272057
Findino Related to Evaluations of Chanqes. Tests, or Exoeriments and Permanent Plant Modifications - Inadequate 50.59 Screen Evaluation for EC272057


=====Introduction:=====
=====Introduction.=====
A Severity Level IV NCV of 10 CFR 50.59(d)(1), "Changes, Tests, and Experiments," was identified because NextEra did not provide an evaluation that adequately documented why implementing a design change to address an identified reduction in the concrete modulus of elasticity for several Category I concrete structures, did not present a more than minimal increase in the likelihood of the occurrence of a malfunction of a structure, system, or component (SSC) important to safety previously evaluated in the updated safety analysis report (USAR). Specifically, NextEra issued EC272057 on April 25, 2011, to address reduced concrete modulus of elasticity in the control building electric tunnel and the containment enclosure building, but did not complete a 10 CFR 50.59 evaluation prior to implementing changes to the facility as described in the modification.
The inspectors identified a Severity Level lV NCV of 10 CFR 50,59(dX1),
"Changes, Tests, and Experiments," because NextEra did not adequately evaluate a "uSe-aS-iS" determination for the ASR impacted Category l concrete structures.


=====Description:=====
Specifically, NextEra did not complete a 10 CFR 50.59 evaluation, to ensure that the identified reduction in concrete modulus of elasticity did not present a more than minimal increase in the likelihood of the occurrence of a malfunction of a SSC important to safety previously evaluated in the updated safety analysis report (USAR) prior to implementing changes to the facility as described in the engineering change EC272057 issued on April25, 2011.
NextEra determined that certain below grade concrete walls were affected by alkali-silica reaction (ASR). The analysis of concrete cores taken from ASR affected areas, showed a reduced concrete modulus of elasticity in the control building / electric tunnel (AR581434), containment enclosure building (AR1644074)and four other seismic Category I buildings (AR1664399).


The lowest measured modulus was about 40% less than the design value of 3.62E+03 ksi.Enclosure 7 On April 25, 2011, NextEra issued EC272057, "Concrete Modulus of Elasticity Evaluation," to address the reduced modulus. EC272057 dispositioned the degraded condition as "use-as-is," and incorporated the degraded condition into the design basis.In a safety evaluation screen for EC272057, NextEra concluded the change did not require a complete evaluation per 50.59(c)(2)because adequate design margin existed and there was no adverse affect on an UFSAR described design function.10 CFR 50.59 requires licensees to evaluate whether NRC approval is required for proposed changes to the facility.
=====Description.=====
On April 25,2011, NextEra issued EC272057, "Concrete Modulus of Elasticity Evaluation," to address the reduced concrete modulus in the CB, the "B" electric tunnel, the containment enclosure building, the diesel generator fuel oil tank rooms, the residual heat removal equipment vaults, and emergency feedwater pump house. EC272057 dispositioned the degraded condition as "use-as-is" and incorporated the degraded condition into the design basis. In a safety evaluation screen for EC272Q57, NextEra concluded the change did not require a complete evaluation per 10 CFR 50.59(c)(2) because adequate design margin existed and there was no adverse affect on an UFSAR described design function.


The Seabrook 5059 Resource Manual defines the process for completing 10 CFR 50.59 evaluations for changes, tests and experiments completed at Seabrook.
a.


It includes a screening process that defines criteria used to determine whether a full 10 CFR 50.59 evaluation must be performed for each applicable change, test or experiment.
b.


NextEra screened EC272057 in accordance with the guidance in the 5059 Resource Manual and concluded that the change did not require a full evaluation per 50.59(c)(2)because adequate design margin existed and there were no adverse affects on the UFSAR described design functions.
c.


The inspectors reviewed EC272057 and determined that NextEra's 50.59 Screen for EC272057 did not correctly address "adverse affects" as described in Section 5.2.2 of the 5059 Resource Manual. The concrete modulus of elasticity is a design value specified in both the Seabrook UFSAR and the ACI 318 Building Code for the applicable plant structures.
10 CFR 50.59 requires licensees to evaluate whether NRC approval is required for proposed changes to the facility. The Seabrook 5059 Resource Manual defines the process for completing 10 CFR 50.59 evaluations for changes, tests, and experiments completed at Seabrook. lt includes a screening process that defines criteria used to determine whether a full 10 CFR 50.59 evaluation must be performed for each applicable change, test, or experiment. NextEra screened EC272057 in accordance with the guidance in the 5059 Resource Manual and concluded that the change did not require a full evaluation per 10 CFR 50.59(cX2) because adequate design margin existed and there were no adverse affects on the UFSAR described design functions.


The reduced modulus of elasticity caused by the ASR occurring in impacted concrete walls has the potential to affect the flexural capacity and dynamic response of the impacted structures.
The inspectors reviewed EC272057 and determined that NextEra's 50.59 Screen for EC272057 did not correctly address "adverse affects" as described in Section 5.2.2 ot the 5059 Resource Manual. The concrete modulus of elasticity is a design value specified in both the Seabrook UFSAR and the ACI 318 - 1971 Building Code for the applicable plant structures. The inspectors determined that the reduced modulus of elasticity caused by the ASR could have had an "adverse affect" on the flexural and dynamic response of the impacted structures and, as such, required further evaluation per 10 CFR 50.59(cX2
: (ii) and (iv). The criterion c(2)(ii) and
: (iv) dealwith the change resulting in more than minimal increase in the likelihood of occurrence or in the consequences of a malfunction of an SSC important to safety previously evaluated in the UFSAR. In response to the inspectors' concerns regarding the adequacy of the 10 CFR 50.59 evaluation, NextEra rescinded the design change EC272057 from the design basis on September 22,2011, and initiated additional evaluations of the ASR affected structures.


Therefore, the inspectors determined that there was sufficient evidence that the reduction in the modulus of elasticity was caused by the ASR and it was an "adverse affect" as described in Section 5.2.2 of the 5059 Resource Manual and thus required further evaluation per 50.59(c)(2).
NextEra personnel did not complete the 10 CFR 50.59 screen properly because they misunderstood the guidance in the 50.59 Resource Manual regarding the need to screen in changes in design parameters which impact the design function acceptance criteria (Resource Manual Section 5.2.2).


The additional evaluation required by 10 CFR 50.59 d(1) was needed to at least ensure that 10 CFR 50.59 c(2) (ii)and
Analvsis. The inspectors determined that the failure to evaluate changes to the facility as described in EC272057 was contrary to 10 CFR 50.59(dX1) and was a performance deficiency warranting a significance evaluation in accordance with the NRC Enforcement Manual for Traditional Enforcement and IMC 0612, "Power Reactor lnspection Reports,"
: (iv) criteria were not met and, therefore, there would be a need for a license amendment per 10 CFR 50.90. The criterion c(2)(ii) and iv) deal with the change resulting in more than minimal increase in the likelihood of occurrence or in the consequences of a malfunction of an SSC important to safety previously evaluated in the UFSAR. In response to the inspectors concerns regarding the adequacy of the 50.59 evaluation, NextEra rescinded the design change EC272057 from the design basis on September 22, 2011, and initiated additional evaluations of the ASR affected structures.
Appendix B, "lssue Disposition Screening." The violation was determined to be more than minor in accordance with IMC 0612, "Power Reactor Inspection Reports,"
Appendix B, "lssue Screening," because the inspector could not reasonably determine that the changes would not have ultimately required prior NRC approval.


On October 14, 2011, NextEra issued additional information to support of its engineering evaluation of the ASR impacted structures, including Calculation C-S-1 -10163, the Prompt Operability Determination for AR581434 (CB/ ET) Revision 1, and the Prompt Operability Determination for AR1664399 (CEB and other Category I Structures)
Violations of 10 CFR 50.59 are dispositioned using the traditional enforcement process instead of the SDP because they are considered to be violations that could potentially impede or impact the regulatory process. However, if possible, the underlying technical issue is evaluated under the SDP to determine the severity of the violation. In this case, for Mitigating Systems, the inspector determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process,"
Revision 1. The reduced modulus caused the concrete to have increased flexure, but the results of NextEra's additional evaluations confirmed that the reduction in capacity was minimal and the resultant stresses on the steel and concrete caused by the ASR degradation remained below the design stress limits with margin. Similarly, the affect of the reduced modulus also reduced the natural frequency of the structures, but the additional evaluation again determined that the shift in natural frequency was minimal and remained well above the ground response peak frequency range such that the response of the structures remained rigid. Therefore, although the effect of the ASR on the impacted walls was to reduce the design modulus parameter, the structural integrity Enclosure remained fully intact under all design loads, and the buildings remained operable.NextEra actions continue to review the degraded concrete issue within the corrective action program, including the effects on the long term reliability of the structures.
0609.04, "Phase 1 - Initial Screening and Characterization of Findings." The issue was determined to be of very low safety significance (Green) because it was a design or qualification deficiency confirmed not to result in an actual loss of safety function, because further evaluation determined that the structures remained operable despite the degraded modulus condition. In accordance with Section 6.1.d.2 of the NRC Enforcement Policy, this violation is categorized as Severity Level lV because the resulting changes were evaluated by the SDP as having very low safety significance (Green). Upon removal of EC272057 from the design basis on September 22, 2011, the issue no longer required an evaluation per 10 CFR 50.59(aX2).


See Section 40A5 of this report for further NRC reviews of the revised operability determinations for ASR impacted structures.
The finding had a cross cutting aspect in the area of human performance - work practices, H.4(b), because NextEra personnel did not follow procedures. Specifically, NextEra personnel did not address "adverse effects" as required by Section 5.2.2 of the 50.59 Resource Manual when preparing the 10 CFR 50.59 screen for EC272057.


Analysis The inspectors determined that the failure to evaluate changes to the facility as described in EC272057 was contrary to 10 CFR 50.59(d)(1)and was a performance deficiency warranting a significance evaluation in accordance with the NRC Enforcement Manual for Traditional Enforcement and Inspection Manual Chapter (IMC) 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Disposition Screening." The violation was determined to be more than minor in accordance with IMC 0612, "Power Reactor Inspection Reports," Appendix B, "Issue Screening," because the inspector could not reasonably determine that the changes would not have ultimately required prior NRC approval.Violations of 10 CFR 50.59 are dispositioned using the Traditional Enforcement process instead of the SDP because they are considered to be violations that could potentially impede or impact the regulatory process. However, if possible, the underlying technical issue is evaluated under the SDP to determine the severity of the violation.
=====Enforcement.=====
 
Title 10 CFR 50.59, "Changes, Tests, and Experiments," Section (dX1)states, in part, that the licensee shall maintain records of changes in the facility or procedures, and that the records must include a written evaluation that provides the bases for the determination that the change does not require a license amendment pursuant to paragraph 10 CFR 50.59(c)(2). Contrary to the above, from April 25 to September 22, 2011, NextEra did not provide an evaluation that adequately documented why the reduced concrete modulus of elasticity in Category l structures did not present a more than minimal increase in the likelihood of occurrence of a malfunction of a SSC important to safety previously evaluated in the USAR. Because this failure to properly evaluate a proposed change is of very low safety significance and has been entered into the licensee's Corrective Action Program (CR1647722), this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.
In this case, the inspector determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process," Attachment 0609.04, "Phase 1 -Initial Screening and Characterization of Findings," Tables 3b and 4a, for the Mitigating Systems Cornerstone.
 
The inspector answered "Yes" to Question 5 under the Mitigating Systems Cornerstone column of the Phase 1 worksheet because the inspector concluded that the finding screened as potentially risk significant due to a design or qualification deficiency confirmed not to result in a loss of operability or functionality.
 
In accordance with Section 6.1 .d.2 of the NRC Enforcement Policy, this violation is categorized as Severity Level IV because the resulting changes were evaluated by the SDP as having very low safety significance (Green). Further evaluation determined that the structures remained operable despite the degraded modulus condition.
 
Upon removal of EC272057 from the design basis on September 22, 2011, the issue no longer required an evaluation per 10 CFR 50.59(a)(2).
 
NextEra personnel did not complete the 50.59 screen properly because they misunderstood the guidance in the 50.59 Resource Manual regarding the need to screen in changes in design parameters which impact the design function acceptance criteria (Resource Manual Section 5.2.2). The finding had a cross cutting aspect in the area of human performance
-work practices, H.4(b), because NextEra personnel did not follow procedures.
 
Specifically, NextEra personnel did not follow the requirements of Section 5.2.2 of the 50.59 Resource Manual when preparing the 50.59 screen for EC272057.Enforcement Title 10 CFR 50.59, "Changes, Tests, and Experiments," Section (d)(1)states, in part, that the licensee shall maintain records of changes in the facility or procedures, and that the records must include a written evaluation that provides the bases for the determination that the change does not require a license amendment pursuant to paragraph 10 CFR 50.59(c)(2).
 
Contrary to the above, from April 25 to September 22, 2011, NextEra did not provide an evaluation that adequately documented why the reduced concrete modulus of elasticity in Category I structures did not present a Enclosure I 9 more than minimal increase in the likelihood of occurrence of a malfunction of a SSC important to safety previously evaluated in the USAR. Because this failure to properly evaluate a proposed change is of very low safety significance and has been entered into the licensee's Corrective Action Program (CR1647722), this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy. (NCV 05000443/2011010-02, Failure to Properly Complete a 5059 Screen for EC272057).
 
==OTHER ACTIVITIES==
40A5 Other Activities
 
===.1 (Closed) Unresolved===
 
Item 05000443/2011003-02, 50.59 Evaluation for Accepting Reduced Modulus of Elasticity in Certain Safety-Related Structures Affected by ASR
 
====a. Inspection Scope====
The inspector reviewed EC272057, dated April 25, 2011, for adequacy in which the EC addressed reduced concrete modulus of elasticity in the control building electric tunnel and the containment enclosure building.
 
The review was to determine if only a 50.59 screening was acceptable to accept "as-is" conditions for this concrete material property which was degraded from the design bases as reflected in the UFSAR.b. Observations/Findings This issue was closed since the inspectors identified one Severity Level IV NCV, as described in Section 1 R1 7 of this report..2 (Open) Unresolved Item 05000443/2011003-03, Open Operability Determinations for Safety-Related Structures Affected by ASR
 
====a. Inspection Scope====
The scope of this review was to update NextEra actions. to date. The inspectors reviewed the prompt operability determination for the control building, and for the extent of conditions review for other buildings affected by the alkali silica reaction.
 
The inspectors utilized site records and interviews to develop the design basis for the safety related structures in greater detail than summarized in section 3.8 of the Updated Final Safety Analysis Report. Additionally, this review was assessed progress in the development of a plan and schedule to address inspection activities, in-situ and laboratory testing to address the alkali-silica-reaction degradation with specific focus on the Control Building as a test case for review.With respect to laboratory conditions the inspector verified:
1) organized and clean working area during both sample preparation (measurements and cutting) and compression testing; 2) adequate lighting available at all times; 3) ambient room temperature
(- 68 0 F) observed during preparation and testing; and 4) core samples were adequately stored and labeled in individual bags. Particular care was taken to ensure only one core was handled at any given time so as not to confuse cores during measurements, cutting, and testing. With respect to equipment calibration, the inspector Enclosure 10 verified:
1) caliper (model 500-505-10, serial #0014816)calibration document and calibration sticker on the caliper; and, 2) compression machine (model CM5000-D, serial#11005) calibration document and calibration sticker on the machine. With respect to test technician qualifications, the inspector also verified qualification records (Level 2 qualification for concrete testing up to date). The inspector also reviewed the Altran Commercial Grade Dedication Plan 10-0076 Part 05 -In Field Check List -the check list was in hand during the preparation and testing.During the week of November 28, 2011, the inspector continued to review historical documentation from the construction phase of the plant, correlation between the concrete strength value determined by the recent core samples and the original strength values determined at the time of concrete placement.
 
The licensee's projected plan and schedule for further studies and assessment of the ASR problem was discussed and reviewed with cognizant engineering and management personnel.
 
The inspectors reviewed the licensee's procedures for administration and control of engineering and testing service vendors and contactors.
 
Additionally, the inspector reviewed the results and documentation of IWL inspection of the containment, and the results of the licensee's efforts in inspection and mapping of 'crazed' cracking in containment and enclosure building wall and the adequacy and validity of the documented results.b. Observations/Findinqs The inspectors identified one finding which was addressed in section 1 R1 5 of this report.In summary of the finding, the operability determinations did not fully evaluate design information that was available on the potential effects of the reduced modulus of elasticity in the following areas: overall stiffness and resulting seismic response, concrete material property changes affecting natural frequency and therefore the amplitude of the seismic response, and the performance of systems and components attached to the affected structures during seismic events. Procedure EN-AA-203-1001 required that these impacts be evaluated as part of the prompt operability determination based on available information.
 
The unresolved item was kept open because the operabilitiy determinations have not been finalized.
 
Several other observations were made in order to update this item. The reviewers noted that NextEra had engaged knowledgeable vendors, appropriate consultants, and recognized experts for testing, analysis, and evaluation of the effects of alkali-silica-reaction, on the serviceability and safety of the affected structures.
 
Although the NextEra plan has not been refined before the NRC staff may be able to determine that if it meets the rigor expected of an Appendix B Quality Assurance program, a preliminary schedule of actions generally consistent with the proposed plans from the contractors was underdevelopment.
 
It was noted that some of the elements of an aging management program had been developed and a final one was under development putting for putting in place, including monitoring and trending.
 
Additional core samples were planned, the operability determination was to be updated as new information, analysis, and assessments became available on an as needed basis. The extent of condition was being comprehensively determined along with building initial assessments through the work of its consultants and contractors.
 
NextEra was also developing and scheduling actions to determine where the alkali-silica-reaction was on the alkali Enclosure 11 depletion curve (relates to extent of potential future degradation), although the tests may take up to two years to complete, and provide reliable data.On October 14, 2011, NextEra issued additional information in support of its engineering evaluation of the alkali-silica-reaction impacted structures, including Calculation C-S-1-10163, the Prompt Operability Determination for AR581434 (for the Control Building and Electrical Tunnel), Revision 1, and the Prompt Operability Determination for AR1664399 (other Category I Structures), Revision 1. In C-S-1-10163, the fundamental frequency was evaluated using the measured modulus of elasticity determined in concrete core samples taken from the building walls. The calculation evaluated the impact of the reduced modulus (compared to the design value) on the wall stiffness with respect to the ground response spectra for the Seabrook site. The building response frequency was calculated using the principles and equations of engineering mechanics for a uniformly loaded fixed-fixed beam model (a simple span fixed at both ends during a seismic event). The effect of the reduced modulus was similarly evaluated to assess the impact on the natural frequency of the structures.
 
The seismic analysis, for Seabrook described in Updated Final Safety Analysis Report Section 3.7(B).2, was used in the design of Category I Structures, systems and components at Seabrook.The inspectors completed a detailed review of C-S-1-10163 and verified that the calculation inputs were supported by plant data and the design references cited in the calculation.
 
No inadequacies were identified.
 
The results of C-S-1-10163 supported NextEra's conclusions in the revised prompt operability determinations, AR 581434 and AR1 664399.Also, during the week of November 14, 2011, a Region III inspector reviewed laboratory testing for compressive strength on fifteen concrete core samples taken from the control building in the October 2011 time frame. The testing was conducted at a laboratory in Northbrook, Illinois.
 
The scope of this review was as noted above. For the testing the week of November 14, 2011, all 15 core samples were compression tested.Photographs were taken for all core samples prior to loading for compression test and after fracture.


Three cores had small length samples cut from them during the cutting phase to be used by Seabrook for further petrography in the near future. Sample preparation (capping)was done in accordance with ASTM C617. Compression testing was done in accordance with ASTM C39. No concerns were noted with respect to quality control during all aspects of compression testing.Other observations were made during the week of November 14, 2011. Multiple laboratory engineers, licensee engineer, and Altran engineer were involved in making call on fracture patterns.
(NCV 050004/32011010-03, Failure to Properly Complete a 50.59 Screen).


All but one of the obtained compressive strengths were fairly consistent with previous lab's results (2010, 2011 data). Core sample L5-C exhibited highest compressive strength of 6610 PSI whereas the previous lab's data identifies strength at 3950 PSI. This core compressive strength value was the only apparent outlier amongst the data set. All 15 destroyed cores are to be shipped back to Seabrook later today including the cut samples to be used for petrography.
4046 Meetinqs. Includins Exit On September 30 and December 2, 2011, the inspectors presented the interim results of this inspection to Mr. P. Freeman, Site Vice President, and Seabrook Station staff. The inspectors also confirmed with NextEra that no proprietary information was retained by inspectors during the course of the inspection.


During the week of November 28, 2011, the IWL Examination Report for the Primary Containment in October 2011, recorded information related to concrete conditions to ensure no unacceptable surface conditions for cracking (greater than 40 mils) and report Enclosure 12 on other conditions such spalling and discoloration conditions.
On January 20,2012, a flnal exit meeting was conducted and led by Mr. Richard J. Conte, Chief Engineering Branch No, 1. Others involved in this conference are noted on the list of contacts. During the meeting, the NRC staff's final disposition of the unresolved items and new findings were summarized. Other comments and questions were communicated to NextEra management with respect to the ASR problem in safety related structures.


Related to this review the inspector noted in AR 01641413 an evaluation of crazed cracking on the exterior surface of the primary containment at azimuth 3150 and elevation
ATTACHMENT: SUPPLEMENTARY I NFORMATION SUPPLEMENTARY I N FORMATION KEY POINTS OF CONTACT Licensee Personnel B. Brown, Supervisor, Civil Engineering V. Brown, Senior Licensing Analyst K. Browne, Plant General Manager J. Esteves, Plant Engineering P. Freeman, Site Vice President P. Gurney, Reactor Engineering Supervisor M. Collins, Manager, Design Engineering M. O'Keefe, Licensing Manager Kev Participants for Teleconference of Januarv 20. 2012 NextEra Attendees:
(-)30 feet, 00 inches.While several factors were identified by NextEra in support of structural integrity of this structure, it was noted the continued evaluation would be done in accordance with the extent of condition review per AR 574120 which identified the loss of concrete strength due to alkali-silica reaction (ASR) in other buildings noted herein. The inspector noted that no specific cause for the crazed cracking was identified which could be due ASR or other mechanisms.
Paul Freeman, Site Vice President Mike O'Keefe, Licensing Manager Mike Collins, Design Engineering Manager Rick Clich6, License Renewal Project Manager Ted Vassallo, Design Engineering Paul Willoughby, Licensing Ken Chew, License Renewal Al Griffith, Public Communications NRC Staff:
Christopher Miller, Division of Reactor Safety, Region I Richard Conte, Division of Reactor Safety, Region I Suresh Chaudhary, Division of Reactor Safety, Region I Art Burritt, Division of Reactor Projects, Region I Bill Raymond, Division of Reactor Projects, Region I John Lamb, Division of Operating Reactor Licensing, NRR Abdul Sheikh, Division of License Renewal, NRR George Thomas, Division of Engineering, NRR Raj Auluck, Division of License Renewal, NRR LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED Opened/Closed:
05000443/201 1-010-01 05000443/201 1-010-02 05000443/201 1 -01 0-03 Closed:
05000443/2011-003-02 Updated:
05000443/201 1 -003-03 URI Adequacy of Corrective Actions Associated with Calculation Methods for Alkali-Silica Reaction lssue FIN lnadequate Operability Determination for Degraded Concrete Structures Housing Safety-Related Equipment NCV Failure to Properly Complete a 50.59 Screen for EC272057 URI Review of 50.59 screening to accept-as-is reduced values for concrete properties in safety related structures.


Further the inspector questioned the reliance on the April 2008 10 CFR 50 Appendix J, Type A Test at 49.6 psig that showed no evidence of cracking greater than 40 mils without the use of a before and after crack mapping effort. No unacceptable conditions were found and the extent of condition review noted above is a part of this open unresolved item.During this inspection, it was determined that NextEra and its contractor were conducting a remodeling effort on the Containment Building (an extent of condition building reviewed in AR 01664399)using current data from core sample and in-situ reviews such as crack mapping etc. The purpose of this remodeling was to conduct a seismic reanalysis to demonstrate the effects of the reduced modulus on structural response because of the unique design of the building and because of the need to address a global response vs. a localized response.
URI Prompt Operability Determination for Safety Related Structures affected by ASR.


The completion of this review was not expected until early 2012. NRC review determined that the initial evaluation for the CEB did not address the response of the entire structure to seismic loading comparable to the methods described in UFSAR 3.8 and how the induced seismic stresses would shift between the concrete and the steel in adjoining sections of the structure.
Definitions (American Concrete Institute (ACl) Terminoloqv)
Poisson's ratio, y: The ratio of transverse strain (perpendicular to the applied load) to the axial strain (in the direction of the applied load).


In response, NextEra pointed out that they began development of an analytical model to reanalyze the CEB using the as-measured elastic modulus (40%reduced) applied to that ASR-impacted sections.
Modulus of Elasticitv. E: The ratio of the normal stress to the corresponding strain for tensile or compressive stress below the proportional limit of the material.


The results of this analysis will be further reviewed as a part of an Engineering Evaluation scheduled to be completed by March 2012.Notwithstanding the acceptable revised operability determination based on available information, the inspectors noted that these determinations listed no assumptions in the applicable sections.
Shear Modulus or Modulus of Riqiditv. G: The ratio of unit shearing stress to the corresponding unit shearing strain.


The inspectors also noted that design basis code ACI 318-1971 was based on empirical data for determining certain parameters that are a part of the design bases. Also Poison's ratio on concrete cores are not being tested or evaluated and this ratio was in the UFSAR. The assumption of this empirical data was that the relationships were for ASR free concrete.
Bulk Modulus. K: The ratio of the change in average stress to the change in unit volume.


Further, based on a review of the implementation schedule from contractor-submitted plans that do not have NextEra approval as of Nov. 2 9 th, the inspectors noted that the plans do not address the following which are directly related to addressing the unwritten assumptions being made in the prompt operability determinations:
Note: The above parameters are four simplified elastic constants defining a material exhibiting "elastic" behavior.


===1. The plans do not appear to test concrete cores for the following ===
Other Definitions:
Stress: The force per unit area (compressiveltensile, transverse or shear).


key design parameters from the design basis code ACI 318-1971, as for tensile and shear strength, rebar bond strength and Poison's ratio.2. The plans do not appear to address nondestructive testing to assess the current progression of the ASR expansion rate before the destructive tests of the concrete cores.Enclosure 13 3. There was a apparent lack a clear framework for concrete core sampling in the buildings to ensure how representative the core sampling addressing the need for random core sampling in distinction to smart sampling on worst case conditions/doing a bounding calculation along addressing the impact of too much core boring and re-grouting on the building structural integrity.
Strain: In a given direction (transverse or axial) is the change in dimension under load to the original dimension in the direction under consideration, Compressive Strenoth: Capacity of a material or structure to withstand axial pushing forces.


===4. The plans do not appear to address potential ===
When the limit of compressive strength is reached, materials fail.


effects of other degradations from an aggressive groundwater environment along with the presence of ASR.In summary at the close of the inspection, NextEra continued to work on: their plans and implementing schedule, building initial assessments along with evaluation results for additional core sampling; identifying the in-situ and out-of-situ testing (concrete core samples and nondestructive testing of concrete core samples) for the structure areas affected by alkali-silica-reaction; need to address key design parameters for the buildings, such as compressive strength, tensile strength, bond strength (between rebar and the concrete), modulus of elasticity and Poisson's Ratio in terms of how alkali-silica-reaction has affected the non-alkali-silica-reaction functional relationship between these parameters per the design code ACI 318-1971; and, remodeling efforts on the Containment Building.Overall, this area remains open pending further project and test plan development by NextEra and further NRC staff review of the final operability determinations on or about March 2012.4OA6 Meetings, Including Exit On September 30 and December 2, 2011, the inspectors presented the interim results of this inspection to Mr. P. Freeman, Site Vice President, and Seabrook Station staff. The inspectors also confirmed with NextEra that no proprietary information was retained by inspectors during the course of the inspection.
Tensile Strenqth: Capacity of a material or structure to withstand axial pulling forces. When the limit of tensile strength is reached, materials fail.


On January 20, 2011 a final exit meeting was conducted and lead by Mr. Richard J.Conte, Chief Engineering Branch No. 1. Others involved in this conference are noted on the list of contacts.
Shear Strenqth: Capacity of a material or structure to withstand forces parallel to a surface area that could cause sliding failure of the material. When the limit of shear strength is reached, materials fail.


During the meeting, the NRC staff's final disposition of the unresolved items and new findings were summarized.
Bond Strenqth: The resistance to separation of mortar and concrete from reinforcing and other materials with which it is in contact.


Other comments and questions were communicated to NextEra Management with respect to the ASR problem in safety related structures.
LIST OF


14 ATTACHMENT:
=DOCUMENTS REVIEWED=


=SUPPLEMENTARY
Prompt Operability Determination (POD) AR 581434, Reduced Concrete Modulus of Elasticity
INFORMATION=
below Grade in 'B' Electrical Tunnel Exterior Walls, Revision 0, June 27,2011, and
Revision 1, October 14,2011
POD AR 1664399, Reduced Concrete Modulus of Elasticity Below Grade in Containment
Building, RHR Equipment Vaults, EFW Pump House, and Diesel Generator
Fuel OilTank Rooms, Revision 0, June 27,2011, and Revision 1, October 14,2011
Catculation C-S-1-10163, Rev. 0, Fundamental Frequency of ASR Effected Walls,
October 14,2011
Calculation C-S-1-10159, Rev. 0,'B'ElectricalTunnel Transverse Shear Evaluation Supplement
to Calculation CD-20
Calculation C-S-1-10150, Rev. 0, Effects of Reduced Modulus of Elasticity -'B' Electrical
Tunnel Exterior Walls
Calculation CD-20-CALC, UE Control and Diesel Generator Building Design of Material
and Walls below Grade for Electrical Tunnel and the Control Building (Original Design
Calculation)
Drawings for Control Building Concrete (ElectricalTunnel) 9763-F-111342,9763-F'111343
and 9763-F-111345
EC 145305, Condition Assessment of Control Building Concrete
AR1641413, Evaluation of Containment with Craze Cracking in Concrete, April 2Q,2011
AR1644074, Concrete Test Results for Containment Enclosure Building, April 21, 2011
AR 574120, Preliminary Test Results of Control Building Concrete
AR 581434 Test Results from Control Building Concrete Modulus Testing (Results of
petrographic analysis of four of the 12 CB cores identified the presence of moderate
to severe ASR in the concrete)
EC250348, Revision 002, Condition Assessment of Building Concrete


ATTACHMENT
AR 01625775, Revision 000, Petrographic Analysis of Concrete Cores from Seabrook Station
SUPPLEMENTARY
System Description No. SD-66, Revision 2, System Description for Structural Design Criteria
INFORMATION
for Public Service Company of New Hampshire, Seabrook Station, Unit Nos. 1 and 2,
KEY POINTS OF CONTACT
3102184.
===Licensee Personnel===
Seabrook UFSAR, Revision 12, Section 3.8.4, Other Seismic Category 1 Structures
: [[contact::B. Brown]], Supervisor, Civil Engineering
Letter dated 6-29-2011 from Richard Plasse, USNRC, to Mr. Paul Freeman, NextEra Energy
: [[contact::V. Brown]], Senior Licensing
Seabrook, LLC - Request for Additional Information for the Review of Seabrook Station
Analyst
License Renewal Application (Specifically Follow-up to RAl B.2.1.31-1 on pages 2-3)
: [[contact::K. Browne]], Plant General Manager
(M11117843380)
: [[contact::J. Esteves]], Plant Engineering
NextEra Energy Letter SBK-L-1 1154 to USNRC dated 8-11-2011, Docket No. 50-443, Seabrook
: [[contact::P. Freeman]], Site Vice President
Station Response to Request for Additional lnformation - NextEra Energy Seabrook
: [[contact::P. Gurney]], Reactor Engineering
License
Supervisor
NextEra Energy Letter SBK-L-1 1063 to USNRC dated 4-14-2011, Docket No. 50-443, Seabrook
: [[contact::M. Collins]], Manager, Design Engineering
Station Response to Request for Additional Information - NextEra Energy Seabrook
: [[contact::M. O'Keefe]], Licensing
License Renewal Application Request for Additional Information - Set 13 (Specifically
Manager Key Manager Participants
Responses to Follow-up to RAl 8.2.1.31-1 and -2 on pages 4-7) (ML11108A1310)
for Teleconference
NextEra Energy Letter SBK-L-10204to USNRC dated 12-17-2010, Docket No. 50-443,
of January 12, 2012 NRC Staff
Seabrook Station Response to Request for Additional Information - NextEra Energy
: [[contact::C. Miller]], Director Division of Reactor Safety (DRS), Region I
Seabrook License RenewalApplication Aging Management Programs (Specifically
: [[contact::R. Conte]], Chief Engineering
Responses to RAI 8.2.1.31-1, -2 and -3 on pages 36-39) (M11035405340)
Branch No. 1, DRS, Region I
AR
: [[contact::A. Burritt]], Chief Reactor Projects Branch No. 3, Region I LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED Opened: 05000443/2011-010-01
ACt
05000443/2011-010-02
ASR
Closed: 05000443/2011-003-02
ASME
Updated 05000443/2011-003-03
CB
Documents
CEB
Reviewed: FIN Inadequate
CFR
Operability
CR
Determination
DRS
for Degraded Concrete Structures
EC
Housing Safety-Related
EN
Equipment NCV Failure to Properly Complete a 50.59 Screen for EC272057 URI Review of 50.59 screening
FIN
to accept-as-is
tMc
reduced values for concrete properties
IP
in safety related structures.
KSI
NCV Prompt Operability
LRA
Determination
NCV
for Safety Related Structures
NRC
affected by ASR.Attachment
LIST OF ACRONYMS
A A-2 LIST OF ACRONYMS AR ????IMC Inspection
Action Request
Manual Chapter NCV Non-Cited
American Concrete Institute
Violation NRC U.S. Nuclear Regulatory
Alkali-Silica Reaction
Commission
American Society of Mechanical Engineers
NRR Nuclear ????TS Technical
Control Building
Specification
Containment Enclosure Building
URI Unresolved
Code of Federal Regulations
Item Attachment
Corrective Action
Division of Reactor Safety
Engineering Change
Procedural Notice for Engineering Department
Finding
Inspection Manual Chapter
Inspection Procedure
Kilo-pounds per square inch
License Renewal Application
Non-Cited Violation
U.S. Nuclear Regulatory Commission
NRR
OD
POD
psi
PSIG
RCA
SDP
SR
SSC
TIA
TS
UFSAR
URI
USAR
Office of Nuclear Reactor Regulation
Operabil ity Determ ination
Prompt Operability Determination
Pounds per square inch (absolute)
Pounds per square inch (gage)
Radiological Controlled Area
Significance Determination Process
Safety Related
Structure, System, or Component
Task lnterface Agreement
Technical Specification
Updated Final Safety Analysis Report
Unresolved ltem
Updated Safety Analysis Report
Attachment
}}
}}

Latest revision as of 20:00, 12 January 2025

IR 05000443-11-010; NextEra Energy Seabrook, LLC; 9/25/2011 - 12/2/2011 Seabrook Station (Problem Identification and Resolution; Follow-up to Operability and Plant Modifications)
ML120480066
Person / Time
Site: Seabrook NextEra Energy icon.png
Issue date: 03/26/2012
From: Chris Miller
Division of Reactor Safety I
To: Freeman P
NextEra Energy Seabrook
References
G20120266, SECY-2012-0196 IR-11-010
Download: ML120480066 (22)


Text

SUBJECT:

SEABROOK STATION - NRC INSPECTION REPORT 05000443/2011010 RELATED TO ALKALI-SILICA REACTION ISSUE IN SAFETY RELATED STRUCTURES

Dear Mr. Freeman:

On January 20,2012, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Seabrook Station. The enclosed inspection report documents the inspection results, which were discussed at the exit meeting with you and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. In conjunction with the follow-up of two unresolved items, the focus of this inspection was a review of activities involving NextEra's analysis and evaluation related to addressing the Alkali-Silica Reaction (ASR) issue occurring in safety related and other important to safety concrete structures. As a part of this inspection, we reviewed your original and revised Prompt Operability Determinations (POD) for certain affected structures.

During the exit meeting, Mr. Richard J. Conte, Chief Engineering Branch 1, summarized the findings and observations. In addition, he discussed NRC observations regarding your planned correCtive actions and assumptions being made in the NextEra operability determinations. The inspectors conctuded that these structures can currently perform their safety related functions despite the observed degradation due to ASR. However the NRC still has concerns associated with long term operability, therefore additional information is needed to determine: 1) how various characteristics of the concrete may be affected by ASR; 2) the related effects on other elements of the structures, such as rebar, due to groundwater in-leakage; and 3) the rate of progression of the ASR in structures at the site. lt is our understanding that these specific areas are being addressed in a comprehensive corrective action plan that was still being finalized by your organization at the end of the inspection.

Therefore, we request that you summarize your plans to address the above issues at a management meeting to be conducted April 23, 2012, at NRC Headquarters in Rockville, MD.

At the meeting you should be prepared to focus on the following technical issues: 1) describe which applicable American Concrete Institute (ACl) 318 code relationships are affected by ASR and your plans to ensure the applicable licensing and design bases remain valid; 2) describe your comprehensive plans to understand the related effects and overall progression of ASR, its cause, and actions to correct and/or mitigate the issue; and, 3) provide a timeline for key actions, including those to address long term operability, how the degradation affects the design basis, and longer term management of the ASR issue. During the meeting we will discuss your overall corrective action plans, including the documents to be submitted to the NRC on the docket.

Also, the report documents two NRC-identified findings of very low significance (Green) one of which involved a violation of NRC requirements, Because of the very low safety significance, and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations, consistent with Section 2.3.2 of the NRC Enforcement Policy. lf you contest any non-cited violations in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with copies to the RegionalAdministrator, Region l; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident lnspector at Seabrook Station. In addition, if you disagree with the cross-cutting aspect assigned to any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region l, and the NRC Resident Inspector at Seabrook.

ln accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390 of the NRC's

"Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records component of the NRC's document system, Agencyrvide Documents Access and Management System (ADAMS). The ADAMS is accessible from the NRC Web site at http:/lwww.nrc.govlreading-rmladams.html (the Public Electronic Reading Room).

Sincerely,

,aA Christopher G. Miller, Director Division of Reactor Safety Docket No.: 50-443 License No.: NPF-86 Enclosure:

lnspection Report No. 050004431201 1010 w/Attachment: Supplemental Information cc w/encl: Distribution via ListServ

SUMMARY OF FINDINGS

lR 0500044312011010;91251201 1 - 121212011; Seabrook Station (Problem ldentification and

Resolution; Follow-up to Operability and Plant Modifications).

This report covers an inspection by regional inspectors and resident staff, with assistance from the Office of Nuclear Reactor Regulation (NRR) structural specialists. Two Green findings were identified. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using lnspection Manual Chapter (lMC) 0609, "Significance Determination Process" (SDP). The cross-cutting aspects for the findings were determined using IMC 0310,

"Components Within Cross-Cutting Areas." Findings for which the SDP does not apply may be Green, or be assigned a severity levelafter NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

Cornerstone: Mitigating Systems

Green.

The inspectors identified a finding in that NextEra failed to fully evaluate potential structural and seismic response impacts in accordance with the requirements in NextEra procedure EN-AA-1001 after identifying a degraded and nonconforming condition related to degraded conditions for some safety related structures due to Alkali-Silica Reaction (ASR).

Specifically, the evaluation did not consider the following effects due to changed properties of concrete, is reflected in reduced values of the modulus of elasticity as measured directly from concrete core samples: 1) building natural frequency in the dynamic response; 2) performance of anchorages and embedment of systems and components attached to the structures; and, 3) shear strength or capacity of affected structures and the dynamic/flexural response especially those buildings without corresponding shear reinforcement'

The failure to conduct adequate prompt operability determinations per procedure EN-AA-203-1001 for degraded and nonconforming conditions associated with ASR was a performance deficiency relative to a self imposed standard. Specifically, the prompt operability determinations conducted following the identification of ASR in safety-related structures did not completely analyze the effects of the reduced modulus of elasticity on the dynamic and flexural response of the structures to seismic events for certain conditions. This performance deficiency was associated with the design control aspect of the Mitigating Systems cornerstone; and, based on a comparison to Example 3.i of Appendix E of IMC 0612, it was determined to be more than minor. Specificatty, the failure to conduct adequate operability determinations adversely affected the Mitigating Systems cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences because it required an additional evaluation to confirm that the design bases was met. The issue was evaluated using IMC 0609, "significance Determination Process," and was determined to be of very low safety significance (Green). Specifically, when evaluated under IMC 0609, Attachment 4, the performance deficiency was a design or qualification deficiency confirmed not to result in an actual loss of safety function. The finding had a cross cutting aspect in the area of problem identification and resolution, P.1(c), related to ensuring that issues potentially impacting nuclear safety are thoroughly evaluated. Specifically, NextEra did not fully evaluate conditions adverse to quality, including evaluating the effects of the reduced concrete modulus of elasticity for impact on operability of the affected structures. (Section 4OA5.1.c)

Severitv Level lV. The inspectors identified a Severity Level lV non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR) 50.59(dX1), "Changes, Tests, and Experiments," because NextEra did not adequately evaluate a "use-as-is" determination, resulting in a defacto design change, for certain ASR impacted safety related structures.

Specifically, NextEra did not complete a 10 CFR 50.59 evaluation, to ensure that the identified reduction in concrete modulus of elasticity did not present a more than minimal increase in the likelihood of the occurrence of a malfunction of a structure, system, or component (SSC)important to safety previously evaluated in the updated safety analysis report (USAR) prior to implementing changes to the facility as described in the engineering change EC272057 issued on April 25,2011.

The failure to evaluate changes to the facility as described in EC272057 was contrary to 10 CFR 50.59(dX1) and was a performance deficiency warranting a significance evaluation in accordance with the NRC Enforcement Manualfor Traditional Enforcement and IMC 0612,

"Power Reactor Inspection Reports," Appendix B, "lssue Disposition Screening." The violation was determined to be more than minor in accordance with IMC 0612, "Power Reactor Inspection Reports," Appendix B, "lssue Screening," because it could not reasonably be determined that the changes would not have ultimately required prior NRC approval. In accordance with Section 6.1.d.2 of the NRC Enforcement Policy, this violation is categorized as Severity Level lV because the resulting changes were evaluated by the SDP as having very low safety significance (Green), because it was a design or qualification deficiency confirmed not to result in an actual loss of safety function and because further evaluation determined that the structures remained operable despite the degraded modulus condition. The finding had a cross cutting aspect in the area of human performance - work practices, H.4(b), because NextEra personnel did not follow procedures. Specifically, NextEra personnel did not follow the requirements of Section 5.2.2 of the 5059 Resource Manual when preparing the 50.59 screen tor EC272057. (Section 4OA5.2.c)iii

REPORT DETAILS

Backqround In June 2009, NextEra conducted walk downs of structures within the scope of license renewal as part of license renewal application preparations. ln June 2010, the License Renewal Application (LRA) was received by the agency. ln October 2010, the NRC staff noted that the licensee was beginning to formulate actions associated with both finalizing the operability determination for the control building (CB) and starting an extent of conditions review of other areas that may be subject to the alkali-silica reaction (ASR) degradation.

The ASR is a chemical reaction in concrete, which occurs over time in the presence of water, between the alkaline cement paste and reactive non-crystalline silica that is found in some common coarse aggregates. In the presence of water, the ASR for.ms a gel that expands, causing micro-craclis that change the physical structural propertiesl of the concrete, including compressive and tensile strength, modulus of elasticity, and Poisson Ratio. At Seabrook the below-grade concrete structures have experienced groundwater infiltration.

ln the summer of 2010, NextEra performed an lmmediate and Prompt Operability Determination (POD) for the CB "B" electrical tunnel structure based on core samples taken from the building, lnspection Report 05000443/2010004, issued November 1, 2010, documented the NRC review of the POD with no findings.

On May 12,2011, Inspection Report 05000443/2011002 identified two non-cited violations (NCV) of very low safety significance related to maintenance rule (Title 10 of the Code of Federal Regulations (10 CFR) 50.65 a(1) and b(2)) monitoring of structures. One of the NCVs related NextEra's failure to properly monitor the structural performance of the CB resulting in degraded conditions - 10 CFR 50.65 (aX1) (NCV 2011-002-01). Also in May 2011, License Renewal Inspection Report 05000443/2011007 (1P71002) reflected an overall inspection result as follows: "Except for Structures Monitoring Program, results support a reasonable assurance determination for license renewal." The structure monitoring program had not addressed the ASR condition.

On August 12, 2011, lnspection Report 05000443/2011003, identified a NCV of very low safety significance related to the untimely operability determinations regarding the extent of condition review for other buildings affected by ASR. The report also identified two unresolved items (URl) related to the operability determinations. Specifically the report identified: 1) the need for additional information related to open operability determinations, one for the CB "8" electrical tunnel, and the other operability determinations for the extent of conditions review for five other areas/structures with evidence of ASR (URl 201 1-003-03); and,2) potential inadequate screening in accordance with 10 CFR 50.59 for accepting the reduced values found on compressive strength and modulus of elasticity for the "B" Electrical Tunnel and the Containment Enclosure Building (URl 201 1-003-02).

1 Material properties defined in the supplemental section of this report ln September 2011, Region I obtained assistance from the Office of Nuclear Reactor Regulation (NRR) through a Task Interface Agreement (TlA) in order to assist in the review of the open PODs.

OTHER ACTIVITIES

4OI2 Problem ldentification and Resolution (71152-1 sample)

Annual Sample: Corrective Actions Associated with Alkali-Silica Reaction in Safetv Related Structures Inspection Scope This review was to assess progress in the development of a corrective plan and implementing schedule to address the ASR degradation issue including: initial assessments of all buildings potentially affected by the problem; root or apparent cause of the problem; control of in-situ testing such as crack mappingiindexing; control of contractor testing and laboratory test facilities in accordance with quality assurance requirements; and any mitigation or long term monitoring actions. The inspectors reviewed laboratory testing to address the ASR degradation with specific focus on the CB ("8" Electrical Tunnel). Laboratory testing was observed during the week of November 14,2011, to ensure proper sample controls, test preparation, and conduct of the test.

During the week of November 28,2011, the inspectors reviewed historical documentation from the construction phase of the plant, correlations between the concrete strength value determined by the recent core samples, and the original strength values determined at the time of concrete placement. The licensee's projected plan and schedule for further studies and assessment of the ASR problem were discussed and reviewed with cognizant engineering and management personnel. lnspectors also reviewed the licensee's control of contractors and laboratory facilities used to analyze concrete core samples. The inspectors reviewed the licensee's procedures for administration and control of engineering and testing service vendors and contactors.

Additionally, the inspector reviewed the results and documentation of American Society of Mechanical Engineers (ASME) Code Section IWL inspection of the containment.

Findinqs and Observations No findings were identified. The inspector noted that a comprehensive corrective action was still under development. NextEra classified this issue as a significant condition adverse to quality and was in the progress of completing a root cause analysis, which was scheduled to be completed in February 2012 in order to support an Engineering Evaluation in March 2012. The inspectors noted that NextEra's plans to date did not address some key issues related to ASR that include but are not limited to:

a.

b.

(1) Need for other concrete core testing (i.e., low stress range stiffness damage tests) to assess expansion-to-date or severity of degradation in the critical direction of the thickness with no rebar ties and lesser resistance to expansion; Basis for the representativeness of concrete core sampling in the buildings for those taken to date and those to be taken, should they occur; lmpact of core boring and re-grouting on the building structural integrity; and Potential effects of other degradation mechanisms from an "aggressive" groundwater environment along with the presence of ASR.

Methods Used in Evaluatinq Structural Inteqritv The NRC staff noted that the methods used in evaluating structural integrity for the selected buildings were based on the correct design basis code ACI 318-1971.

However, the mathematical relationships in this code were based on empiricaldata, from testing of non-degraded concrete, for determining key ratios that are a part of the design bases and used for determining tensile and shear strength or capacity in addition to compressive strength. These strength values were important in the building loading analysis during normal or upset conditions such as for seismic events. More importantly, while some testing for the modulus of elasticity was done, it was not clear if the plans would result in additional testing of concrete cores for this parameter or any independent testing associated with other key design parameters such as Poisson's Ratio, shear modulus, or bulk modulus. With these parameters known, various strengths or capacities can be determined such as for tensile and shear strength. In addition, the plans that the inspectors reviewed did not address variation in mechanical properties of the concrete in different directions due to ASR cracking nor the effect of the ASR expansion on stresses in the rebar. These parameters were important in order to ensure that the current licensing and design basis was maintained. The licensee representatives agreed to address the assumptions or establish relationships for the current conditions at Seabrook. Accordingly this area is unresolved pending completion of license actions as noted above and further NRC staff review (URf 05000 4/.312011 01 0-01, Corrective Actions Associated with calculation methods used to address the ASR lssue)

Control of ContractorsA/endors and Laboratorv Testinq The reviewers noted that NextEra had engaged knowledgeable vendors, appropriate consultants, and experts for testing, analysis, and evaluation of the effects of ASR on the serviceability and safety of the affected structures. Also, during the week of November 14,2011, a Region lll inspectorreviewed laboratorytestingforcompressive strength on 15 concrete core samples taken from the CB "8" electricaltunnel in the October 2011 time frame. This testing was being completed to resolve discrepant information for compressive strength testing between two different contractors.

The testing was conducted at a laboratory in Northbrook, lllinois. All 15 core samples were compression tested. Photographs were taken for all core samples prior to loading for compression test and after fracture. Three cores had small length samples cut from them to be used by Seabrook for further petrography. Sample preparation (capping)was done in accordance with American Society for Testing and Materials (ASTM) C617.

(2)

(s)

(4) 40A5 Compression testing was done in accordance with ASTM C39. With respect to laboratory conditions for testing of concrete cores, the inspector verified: 1) organized and clean working area during both sample preparation (measurements and cutting)and compression testing; 2) adequate lighting available at all times; 3) ambient room temperature (- 68"F) observed during preparation and testing; and 4) core samples were adequately stored and labeled in individual bags.

The inspector observed the care taken to ensure only one core was handled at any given time so as not to confuse cores during measurements, cutting, and testing. With respect to equipment calibration, the inspector verified proper equipment documentation and calibration. With respect to test technician qualifications, the inspector also verified qualification records. The inspector also reviewed the Altran Commercial Grade Dedication Plan.

No concerns were noted with respect to quality control during all aspects of compression testing. All 15 destroyed cores were shipped back to Seabrook including the cut samples to be used for petrography. These results were to be evaluated by NextEra.

Other Activities (Open) Unresolved ltem 05000443/2011003-03. Open Operabilitv Determinations for Safetv-Related Stru ctu res Affected bv Al kal i-Sil ica Reaction Insoection Scope The NRC staff reviewed NextEra actions to develop finalized operability determinations along with the review for extent of conditions. The review included the open aspects as documented in the originating inspection report for which NextEra was to provide additional information related to: 1) effect of the reduced modulus of elasticity on natural frequency of the structures (applied to CB - "8" Electrical tunnel and other structures being evaluated in the extent of conditions review such as for the Containment Building (CEB); 2) the effect of the modulus of elasticity on structure flexural response as related to components attached to the structures, such as pipe and cable trays supports and their anchor bolts; 3) related effects from increased flexure of building on the loading and seismic effects on safety related pipes and cable tray supports; and, 4) effect of reduced parameters on the whole building (global) response of the CEB structure to seismic loads including further information of the effect on stress and strain in the concrete and rebar system. With respect to numbers 1 and 2 above, the inspectors reviewed the operability determinations for the below listed safety related structures degraded by ASR. The inspectors verified the basis for why the Radiological Control Area tunnel was confirmed to not be affected by ASR. The inspectors reviewed operability determinations for the following buildings:

.1 a.

. Control Building - "8" Electrical Tunnel, o Containment Enclosure Building,

. Diesel Generator Fuel OilTank Rooms,

. Residual Heat Removal Equipment Vaults, and r Emergency Feedwater Pump House.

The inspectors utilized site records and interviews to determine the design basis for the safety related structures in addition to those summarized in Sections 3.7 and 3.8 of the Updated Final Safety Analysis Report (UFSAR).

b. Observations For the open aspects of numbers 1 and 2 above, a finding was identified and addressed in Section 4OA5.1.c. This section also noted a new issue identified by NRC staff related to shear reinforcement for the walls of the CB and the diesel generator building.

The open aspects of numbers 3 and 4 were updated but not completely resolved due to the need to obtain additional information. At the beginning of the inspection, the NRC staff review determined that the initial evaluation for the CEB did not address the open aspects of numbers 1 and 2 above; and, in particular, the response of the entire structure (whole building) to seismic loading comparable to the methods described in UFSAR 3.8. This included how the induced seismic stresses would shift between the concrete and the steel in adjoining sections of the structure. In response, NextEra noted that these issues would be factored into the analytical model (finite element analysis) to reanalyze the CEB using the as-measured worst case elastic modulus applied to ASR-lm pacted sections.

Revision 1 of the applicable operability determination for the CEB provided additional quantitative and qualitative analysis, for the available information, which addressed groundwater intrusion limited to less than 25 percent of the perimeter of the below grade portion of the building; the effect of the reduced modulus on the natural frequency; and the effect on shear capacity that indicated that the dynamic and flexural response had a minimaleffect.

In conclusion, this area remained open pending further developments and completion of licensee actions as noted above and further NRC staff review. While this unresolved item remains open, the NRC staff determined that the affected safety-related structures can currently perform their safety functions. This conclusion was based on the following:

. Conservative safety load factors in controlling load conditions and engineering conservatisms in design provide reasonable expectation that affected structures can perform their safety function, despite the current licensing basis design margin being reduced by the change of mechanical properties;

. Field walk-downs confirm no visible indication of significant deformation, distortion, or displacement of structures, or rebar corrosion;

. Evidence of ASR limited to localized areas in the concrete walls; and

. Progression of ASR degradation occurs slowly based on existing operating experience and published literature, and the licensee continues to monitor.

This unresolved item related to operability of ASR affected safety related buildings remained open for NextEra to evaluate ASR effect on cable and pipe loadings (number 3) and evaluate ASR effect on the CEB whole building response (number 4).

c. Findinq Related to Operabilitv Determinations and Functionalitv Assessments -

Inadequate Operabilitv Determinations lntroduction. The inspector identified a finding in that NextEra failed to fully evaluate potential structural and seismic response impacts in accordance with the requirements in NextEra Procedure EN-AA-1001 after identifying degraded and nonconforming condition related to reduced concrete modulus of elasticity due to ASR degradation for safety related structures. The evaluation did not consider the following effects due to changed properties of concrete as measured directly from building concrete core samples:

building natural frequency in the dynamic response; performance of anchorages and embedment of systems and components attached to the structures; and shear strength or capacity of affected structures and the dynamic/flexural response especially for those building walls without corresponding shear reinforcement.

Description.

NextEra analysis of concrete cores samples taken following the April 2011 determination that certain below grade concrete walls in safety related structures were affected by ASR, indicated a reduced modulus of elasticity and compressive strength.

Although the compressive strength reduction was viewed by NextEra as slight and acceptable, the lowest measured modulus was about 40 percent less than the design value of 3,620 kpsi.

NextEra completed operability determinations for certain affected safety-related concrete structures as required by NextEra Procedure EN-AA-203-1001, "Operability DeterminationsiFunctional Assessments." ln accordance with the Procedure EN-AA-203-1001, an operability determination must include: identification of current licensing basis functions and performance requirements as listed in the UFSAR; identification of the minimum design basis values necessary to satisfy the structure, system, or component (SSC) design basis safety functions; and evaluation of the effects of the degraded condition on the ability of the SSCs to meet its specified function and performance requirements.

During the week of September 26,2011, NRC staff determined that the completed operability determinations were not sufficient in that they did not address the impact of the degraded condition on key aspects of the structure design as described in UFSAR.

Specifically, NextEra failed to address the ASR induced effects of the reduced modulus of elasticity on seismic dynamic and flexural response in the following areas:

r Building naturalfrequency in the dynamic response;

. Performance of anchorages and embedment of systems and components attached to the structures affected by ASR; and

. Shear capacity of affected walls especially for those buildings without corresponding shear reinforcement such as for the CB and the emergency diesel generator building.

NextEra performed additional reviews and updated the operability determinations for the affected areas in response to these concerns, on October 14,2011. The licensee determined that the structures and other affected systems and components remained functional for design basis conditions but were degraded.

The NRC reviewed the updated operability determinations and associated calculations determining that the additional areas needing evaluation were addressed and that the structures remained "operable but degraded." The previous determination indicated that the evaluated structures were "operable." Specifically, NextEra used quantitative and qualitative information with respect to the degraded concrete conditions as noted below.

With respect to dynamic response and the change in the natural frequency of the structures, licensee's additional evaluation determined that the shift in naturalfrequency was minimal and remained well above the ground response peak frequency range such that the response of the structures remained rigid. With respect to the ability of the equipment anchors and embedment to perform their function, the licensee's additional evaluation noted that there was no appreciable impact. The licensee also determined that the impact on the flexural capacity of seismic buildings with respect to shear stress was minimal, and the resultant stresses on the steel and concrete remained below the design stress limits with margin.

Following review, the inspector determined there was a reasonable expectation that the structural integrity remained intact under design loads, and the buildings remained operable but degraded. NextEra continued to review the degraded concrete issue within the corrective action program, including the effects on the long term reliability of the structures.

Analvsis. The inspectors determined that NextEra's failure to conduct adequate prompt operability determinations per Procedure EN-M-203-1001 for degraded and nonconforming conditions associated with ASR was a performance deficiency relative to a self imposed standard. Specifically, the operability determinations conducted following identification of ASR in safety-related structures did not completely analyze the effects of the reduced modulus on the dynamic and flexural response of safety related structures to seismic events along with the effect on attached systems and components. This performance deficiency was associated with the design control aspect of the Mitigating Systems cornerstone; and, based on a comparison to Example 3.i of Appendix E of IMC 0612, it was determined to be more than minor. The issue was evaluated using IMC 0609, "significance Determination Process," and was determined to be of very low safety significance (Green). The finding had a cross cutting aspect in the area of problem identification and resolution, P.1(c), related to ensuring that issues potentially impacting nuclear safety are thoroughly evaluated. NextEra did not thoroughly evaluate conditions adverse to quality, including evaluating the effects of the reduced concrete modulus for impact on operability of the affected structures.

===.2

Enforcement.

Because this finding does not involve a violation and has very low safety===

significance, it is identified as FIN 05000443/2011-10-02, lncomplete Operability Determ i nation for Degraded Concrete Stru ctu res Hous i n g Safety-Re lated Equipment.

(Closed) Unresolved ltem 05000443/201 1003-02. 50.59 Evaluation for Acceptinq Reduced Modulus of Elasticitv in Certain Safetv-Related Structures Affected bv Alkali-Silica Reaction Inspection Scope As part of the review of this unresolved item, the inspectors continued to review EC272057, dated April 25, 2011, for adequacy in which the engineering change (EC)was a design change to address reduced concrete modulus of elasticity in the CB electric tunnel and the containment enclosure building. The review was to determine if only a 10 CFR 50.59 screening was adequate to accept "as-is" conditions for this concrete material property. The inspector reviewed NextEra's revocation of this EC, Observations This issue was closed based on the revocation of the EC, and on the Severity Level lV NCV, as noted below.

Findino Related to Evaluations of Chanqes. Tests, or Exoeriments and Permanent Plant Modifications - Inadequate 50.59 Screen Evaluation for EC272057

Introduction.

The inspectors identified a Severity Level lV NCV of 10 CFR 50,59(dX1),

"Changes, Tests, and Experiments," because NextEra did not adequately evaluate a "uSe-aS-iS" determination for the ASR impacted Category l concrete structures.

Specifically, NextEra did not complete a 10 CFR 50.59 evaluation, to ensure that the identified reduction in concrete modulus of elasticity did not present a more than minimal increase in the likelihood of the occurrence of a malfunction of a SSC important to safety previously evaluated in the updated safety analysis report (USAR) prior to implementing changes to the facility as described in the engineering change EC272057 issued on April25, 2011.

Description.

On April 25,2011, NextEra issued EC272057, "Concrete Modulus of Elasticity Evaluation," to address the reduced concrete modulus in the CB, the "B" electric tunnel, the containment enclosure building, the diesel generator fuel oil tank rooms, the residual heat removal equipment vaults, and emergency feedwater pump house. EC272057 dispositioned the degraded condition as "use-as-is" and incorporated the degraded condition into the design basis. In a safety evaluation screen for EC272Q57, NextEra concluded the change did not require a complete evaluation per 10 CFR 50.59(c)(2) because adequate design margin existed and there was no adverse affect on an UFSAR described design function.

a.

b.

c.

10 CFR 50.59 requires licensees to evaluate whether NRC approval is required for proposed changes to the facility. The Seabrook 5059 Resource Manual defines the process for completing 10 CFR 50.59 evaluations for changes, tests, and experiments completed at Seabrook. lt includes a screening process that defines criteria used to determine whether a full 10 CFR 50.59 evaluation must be performed for each applicable change, test, or experiment. NextEra screened EC272057 in accordance with the guidance in the 5059 Resource Manual and concluded that the change did not require a full evaluation per 10 CFR 50.59(cX2) because adequate design margin existed and there were no adverse affects on the UFSAR described design functions.

The inspectors reviewed EC272057 and determined that NextEra's 50.59 Screen for EC272057 did not correctly address "adverse affects" as described in Section 5.2.2 ot the 5059 Resource Manual. The concrete modulus of elasticity is a design value specified in both the Seabrook UFSAR and the ACI 318 - 1971 Building Code for the applicable plant structures. The inspectors determined that the reduced modulus of elasticity caused by the ASR could have had an "adverse affect" on the flexural and dynamic response of the impacted structures and, as such, required further evaluation per 10 CFR 50.59(cX2

(ii) and (iv). The criterion c(2)(ii) and
(iv) dealwith the change resulting in more than minimal increase in the likelihood of occurrence or in the consequences of a malfunction of an SSC important to safety previously evaluated in the UFSAR. In response to the inspectors' concerns regarding the adequacy of the 10 CFR 50.59 evaluation, NextEra rescinded the design change EC272057 from the design basis on September 22,2011, and initiated additional evaluations of the ASR affected structures.

NextEra personnel did not complete the 10 CFR 50.59 screen properly because they misunderstood the guidance in the 50.59 Resource Manual regarding the need to screen in changes in design parameters which impact the design function acceptance criteria (Resource Manual Section 5.2.2).

Analvsis. The inspectors determined that the failure to evaluate changes to the facility as described in EC272057 was contrary to 10 CFR 50.59(dX1) and was a performance deficiency warranting a significance evaluation in accordance with the NRC Enforcement Manual for Traditional Enforcement and IMC 0612, "Power Reactor lnspection Reports,"

Appendix B, "lssue Disposition Screening." The violation was determined to be more than minor in accordance with IMC 0612, "Power Reactor Inspection Reports,"

Appendix B, "lssue Screening," because the inspector could not reasonably determine that the changes would not have ultimately required prior NRC approval.

Violations of 10 CFR 50.59 are dispositioned using the traditional enforcement process instead of the SDP because they are considered to be violations that could potentially impede or impact the regulatory process. However, if possible, the underlying technical issue is evaluated under the SDP to determine the severity of the violation. In this case, for Mitigating Systems, the inspector determined the finding could be evaluated using the SDP in accordance with IMC 0609, "Significance Determination Process,"

0609.04, "Phase 1 - Initial Screening and Characterization of Findings." The issue was determined to be of very low safety significance (Green) because it was a design or qualification deficiency confirmed not to result in an actual loss of safety function, because further evaluation determined that the structures remained operable despite the degraded modulus condition. In accordance with Section 6.1.d.2 of the NRC Enforcement Policy, this violation is categorized as Severity Level lV because the resulting changes were evaluated by the SDP as having very low safety significance (Green). Upon removal of EC272057 from the design basis on September 22, 2011, the issue no longer required an evaluation per 10 CFR 50.59(aX2).

The finding had a cross cutting aspect in the area of human performance - work practices, H.4(b), because NextEra personnel did not follow procedures. Specifically, NextEra personnel did not address "adverse effects" as required by Section 5.2.2 of the 50.59 Resource Manual when preparing the 10 CFR 50.59 screen for EC272057.

Enforcement.

Title 10 CFR 50.59, "Changes, Tests, and Experiments," Section (dX1)states, in part, that the licensee shall maintain records of changes in the facility or procedures, and that the records must include a written evaluation that provides the bases for the determination that the change does not require a license amendment pursuant to paragraph 10 CFR 50.59(c)(2). Contrary to the above, from April 25 to September 22, 2011, NextEra did not provide an evaluation that adequately documented why the reduced concrete modulus of elasticity in Category l structures did not present a more than minimal increase in the likelihood of occurrence of a malfunction of a SSC important to safety previously evaluated in the USAR. Because this failure to properly evaluate a proposed change is of very low safety significance and has been entered into the licensee's Corrective Action Program (CR1647722), this violation is being treated as an NCV, consistent with Section 2.3.2 of the NRC Enforcement Policy.

(NCV 050004/32011010-03, Failure to Properly Complete a 50.59 Screen).

4046 Meetinqs. Includins Exit On September 30 and December 2, 2011, the inspectors presented the interim results of this inspection to Mr. P. Freeman, Site Vice President, and Seabrook Station staff. The inspectors also confirmed with NextEra that no proprietary information was retained by inspectors during the course of the inspection.

On January 20,2012, a flnal exit meeting was conducted and led by Mr. Richard J. Conte, Chief Engineering Branch No, 1. Others involved in this conference are noted on the list of contacts. During the meeting, the NRC staff's final disposition of the unresolved items and new findings were summarized. Other comments and questions were communicated to NextEra management with respect to the ASR problem in safety related structures.

ATTACHMENT: SUPPLEMENTARY I NFORMATION SUPPLEMENTARY I N FORMATION KEY POINTS OF CONTACT Licensee Personnel B. Brown, Supervisor, Civil Engineering V. Brown, Senior Licensing Analyst K. Browne, Plant General Manager J. Esteves, Plant Engineering P. Freeman, Site Vice President P. Gurney, Reactor Engineering Supervisor M. Collins, Manager, Design Engineering M. O'Keefe, Licensing Manager Kev Participants for Teleconference of Januarv 20. 2012 NextEra Attendees:

Paul Freeman, Site Vice President Mike O'Keefe, Licensing Manager Mike Collins, Design Engineering Manager Rick Clich6, License Renewal Project Manager Ted Vassallo, Design Engineering Paul Willoughby, Licensing Ken Chew, License Renewal Al Griffith, Public Communications NRC Staff:

Christopher Miller, Division of Reactor Safety, Region I Richard Conte, Division of Reactor Safety, Region I Suresh Chaudhary, Division of Reactor Safety, Region I Art Burritt, Division of Reactor Projects, Region I Bill Raymond, Division of Reactor Projects, Region I John Lamb, Division of Operating Reactor Licensing, NRR Abdul Sheikh, Division of License Renewal, NRR George Thomas, Division of Engineering, NRR Raj Auluck, Division of License Renewal, NRR LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED Opened/Closed:

05000443/201 1-010-01 05000443/201 1-010-02 05000443/201 1 -01 0-03 Closed:

05000443/2011-003-02 Updated:

05000443/201 1 -003-03 URI Adequacy of Corrective Actions Associated with Calculation Methods for Alkali-Silica Reaction lssue FIN lnadequate Operability Determination for Degraded Concrete Structures Housing Safety-Related Equipment NCV Failure to Properly Complete a 50.59 Screen for EC272057 URI Review of 50.59 screening to accept-as-is reduced values for concrete properties in safety related structures.

URI Prompt Operability Determination for Safety Related Structures affected by ASR.

Definitions (American Concrete Institute (ACl) Terminoloqv)

Poisson's ratio, y: The ratio of transverse strain (perpendicular to the applied load) to the axial strain (in the direction of the applied load).

Modulus of Elasticitv. E: The ratio of the normal stress to the corresponding strain for tensile or compressive stress below the proportional limit of the material.

Shear Modulus or Modulus of Riqiditv. G: The ratio of unit shearing stress to the corresponding unit shearing strain.

Bulk Modulus. K: The ratio of the change in average stress to the change in unit volume.

Note: The above parameters are four simplified elastic constants defining a material exhibiting "elastic" behavior.

Other Definitions:

Stress: The force per unit area (compressiveltensile, transverse or shear).

Strain: In a given direction (transverse or axial) is the change in dimension under load to the original dimension in the direction under consideration, Compressive Strenoth: Capacity of a material or structure to withstand axial pushing forces.

When the limit of compressive strength is reached, materials fail.

Tensile Strenqth: Capacity of a material or structure to withstand axial pulling forces. When the limit of tensile strength is reached, materials fail.

Shear Strenqth: Capacity of a material or structure to withstand forces parallel to a surface area that could cause sliding failure of the material. When the limit of shear strength is reached, materials fail.

Bond Strenqth: The resistance to separation of mortar and concrete from reinforcing and other materials with which it is in contact.

LIST OF

DOCUMENTS REVIEWED

Prompt Operability Determination (POD) AR 581434581434 Reduced Concrete Modulus of Elasticity

below Grade in 'B' Electrical Tunnel Exterior Walls, Revision 0, June 27,2011, and

Revision 1, October 14,2011

POD AR 1664399, Reduced Concrete Modulus of Elasticity Below Grade in Containment

Building, RHR Equipment Vaults, EFW Pump House, and Diesel Generator

Fuel OilTank Rooms, Revision 0, June 27,2011, and Revision 1, October 14,2011

Catculation C-S-1-10163, Rev. 0, Fundamental Frequency of ASR Effected Walls,

October 14,2011

Calculation C-S-1-10159, Rev. 0,'B'ElectricalTunnel Transverse Shear Evaluation Supplement

to Calculation CD-20

Calculation C-S-1-10150, Rev. 0, Effects of Reduced Modulus of Elasticity -'B' Electrical

Tunnel Exterior Walls

Calculation CD-20-CALC, UE Control and Diesel Generator Building Design of Material

and Walls below Grade for Electrical Tunnel and the Control Building (Original Design

Calculation)

Drawings for Control Building Concrete (ElectricalTunnel) 9763-F-111342,9763-F'111343

and 9763-F-111345

EC 145305, Condition Assessment of Control Building Concrete

AR1641413, Evaluation of Containment with Craze Cracking in Concrete, April 2Q,2011

AR1644074, Concrete Test Results for Containment Enclosure Building, April 21, 2011

AR 574120574120 Preliminary Test Results of Control Building Concrete

AR 581434581434Test Results from Control Building Concrete Modulus Testing (Results of

petrographic analysis of four of the 12 CB cores identified the presence of moderate

to severe ASR in the concrete)

EC250348, Revision 002, Condition Assessment of Building Concrete

AR 01625775, Revision 000, Petrographic Analysis of Concrete Cores from Seabrook Station

System Description No. SD-66, Revision 2, System Description for Structural Design Criteria

for Public Service Company of New Hampshire, Seabrook Station, Unit Nos. 1 and 2,

3102184.

Seabrook UFSAR, Revision 12, Section 3.8.4, Other Seismic Category 1 Structures

Letter dated 6-29-2011 from Richard Plasse, USNRC, to Mr. Paul Freeman, NextEra Energy

Seabrook, LLC - Request for Additional Information for the Review of Seabrook Station

License Renewal Application (Specifically Follow-up to RAl B.2.1.31-1 on pages 2-3)

(M11117843380)

NextEra Energy Letter SBK-L-1 1154 to USNRC dated 8-11-2011, Docket No. 50-443, Seabrook

Station Response to Request for Additional lnformation - NextEra Energy Seabrook

License

NextEra Energy Letter SBK-L-1 1063 to USNRC dated 4-14-2011, Docket No. 50-443, Seabrook

Station Response to Request for Additional Information - NextEra Energy Seabrook

License Renewal Application Request for Additional Information - Set 13 (Specifically

Responses to Follow-up to RAl 8.2.1.31-1 and -2 on pages 4-7) (ML11108A1310)

NextEra Energy Letter SBK-L-10204to USNRC dated 12-17-2010, Docket No. 50-443,

Seabrook Station Response to Request for Additional Information - NextEra Energy

Seabrook License RenewalApplication Aging Management Programs (Specifically

Responses to RAI 8.2.1.31-1, -2 and -3 on pages 36-39) (M11035405340)

AR

ACt

ASR

ASME

CB

CEB

CFR

CR

DRS

EC

EN

FIN

tMc

IP

KSI

LRA

NCV

NRC

LIST OF ACRONYMS

Action Request

American Concrete Institute

Alkali-Silica Reaction

American Society of Mechanical Engineers

Control Building

Containment Enclosure Building

Code of Federal Regulations

Corrective Action

Division of Reactor Safety

Engineering Change

Procedural Notice for Engineering Department

Finding

Inspection Manual Chapter

Inspection Procedure

Kilo-pounds per square inch

License Renewal Application

Non-Cited Violation

U.S. Nuclear Regulatory Commission

NRR

OD

POD

psi

PSIG

RCA

SDP

SR

SSC

TIA

TS

UFSAR

URI

USAR

Office of Nuclear Reactor Regulation

Operabil ity Determ ination

Prompt Operability Determination

Pounds per square inch (absolute)

Pounds per square inch (gage)

Radiological Controlled Area

Significance Determination Process

Safety Related

Structure, System, or Component

Task lnterface Agreement

Technical Specification

Updated Final Safety Analysis Report

Unresolved ltem

Updated Safety Analysis Report

Attachment