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{{#Wiki_filter:(ACCELERATED
{{#Wiki_filter:(ACCELERATED
RIDSPROCESSING)
RIDS PROCESSING)
REGULATORY
R EGULATORY INFORMATION
INFORMATION
DISTRIBUTION
DISTRIBUTION
SYSTEM(RIDS)'CESSIONNBR:9408240071
SYSTEM (RIDS)'CESSION NBR:9408240071
DOC.DATE:
DOC.DATE: 94/08/19 NOTARIZED:
94/08/19NOTARIZED:
YES DOCKET FACIL:50-315
YESDOCKETFACIL:50-315
Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH.NAME AUTHOR AFFILIATION
DonaldC.CookNuclearPowerPlant,Unit1,IndianaM0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,IndianaM05000316AUTH.NAMEAUTHORAFFILIATION
FITZPATRICK,E.
FITZPATRICK,E.
IndianaMichiganPowerCo.(formerly
Indiana Michigan Power Co.(formerly Indiana&Michigan Ele RECIP.NAME
Indiana&MichiganEleRECIP.NAME
RECIPIENT AFFILIATION
RECIPIENT
Document Control Branch (Document Control Desk)SUBJECT: Responds to NRC 940720 ltr re violations
AFFILIATION
noted in insp rept 50-315/94-13
DocumentControlBranch(Document
ControlDesk)SUBJECT:RespondstoNRC940720ltrreviolations
notedininsprept50-315/94-13
&50-316/94-13.Corrective
&50-316/94-13.Corrective
actions:work
actions:work
controlprocesscodewaschangedon2-MMO-240
control process code was changed on 2-MMO-240 repair job order&PMI-7030 will be revised to redefine rework.DISTRIBUTION
repairjoborder&PMI-7030willberevisedtoredefinerework.DISTRIBUTION
CODE: IE01D COPIES RECEIVED:LTR
CODE:IE01DCOPIESRECEIVED:LTR
ENCL SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice
ENCLSIZE:TITLE:General(50Dkt)-Insp
of Vio ation Response NOTES: RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD/DE I B AEOD/S PD/RRAB DEDRO NRR/DRCH/HHFB, NUDOCS-ABSTRACT
Rept/Notice
OGC/HDS2 RES/HFB EXTERNAL EG&G/BRYCE i J~H~NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME HICKMAN,J AEOD/SPD/RAB
ofVioationResponseNOTES:RECIPIENT
AEOD/TTC NRR/DORS/OEAB
IDCODE/NAME
PD3-1PDINTERNAL:
AEOD/DEIBAEOD/SPD/RRABDEDRONRR/DRCH/HHFB,
NUDOCS-ABSTRACT
OGC/HDS2RES/HFBEXTERNALEG&G/BRYCEiJ~H~NRCPDRCOPIESLTTRENCL11111111111111111111RECIPIENT
IDCODE/NAME
HICKMAN,J
AEOD/SPD/RAB
AEOD/TTCNRR/DORS/OEAB
NRR/PMAS/IRCB-E
NRR/PMAS/IRCB-E
0RREGFIL02GN3FILE01NOACCOPIESLTTRENCL111111111111111111NOTETOALL"RIDS"RECIPIENTS:
0 R REG FIL 02 GN3 FILE 01 NOAC COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASEHELPUSTOREDUCEiVASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2083)TOELIMINATE
PLEASE HELP US TO REDUCE iVASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.504-2083)TO ELIMINATE YOUR NAME F ROTI DISTRIBUTION
YOURNAMEFROTIDISTRIBUTION
LISTS FOR DOCUMENTS YOU DON"I'EED!TOTAL NUMBER OF COPIES REQUIRED'TTR
LISTSFORDOCUMENTS
19 ENCL 19
YOUDON"I'EED!TOTALNUMBEROFCOPIESREQUIRED'TTR
19ENCL19
   
   
IndianaMichiganPowerCompanyP.O.Box16631Columbus,
Indiana Michigan Power Company P.O.Box 16631 Columbus, OH 43216 INDIANA NICHIGAN POWER AEP;NRC'1212G
OH43216INDIANANICHIGANPOWERAEP;NRC'1212G
10 CFR 2.201 Donald C.Cook Nuclear Plant Units 1 and 2 Docket Nos.50-315 and 50-316 License Nos.DPR-58 and DPR-74 NRC INSPECTION
10CFR2.201DonaldC.CookNuclearPlantUnits1and2DocketNos.50-315and50-316LicenseNos.DPR-58andDPR-74NRCINSPECTION
REPORTS NO.50-315/94013 (DRP)AND 50-316/94013 (DRP)REPLY TO NOTICE OF VIOLATION U.S.Nuclear Regulatory
REPORTSNO.50-315/94013
(DRP)AND50-316/94013
(DRP)REPLYTONOTICEOFVIOLATION
U.S.NuclearRegulatory
Commission
Commission
DocumentControlDeskWashington,
Document Control Desk Washington, D.C.20555 Attn: Mr.J.B.Martin August 19, 1994 Dear Mr.Martin: This letter is in response to a USNRC letter dated July 20, 1994, that forwarded a notice of violation to Indiana Michigan Power Company.The notice of violation contained one violation identified
D.C.20555Attn:Mr.J.B.MartinAugust19,1994DearMr.Martin:ThisletterisinresponsetoaUSNRCletterdatedJuly20,1994,thatforwarded
during a routine safety inspection
anoticeofviolation
conducted by Messrs.J.A.Isom, D.J.Hartland, and D.L.Shepard from June 4, 1994, through July 1, 1994.The violation is associated
toIndianaMichiganPowerCompany.Thenoticeofviolation
with the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions
contained
of operation.
oneviolation
Our reply to the notice of violation is provided in the attachment
identified
to this letter.This letter is submitted pursuant to 10 CFR 50.54(f)and, as such, an oath statement is attached.p~W)Vice President ar Attachment
duringaroutinesafetyinspection
conducted
byMessrs.J.A.Isom,D.J.Hartland,
andD.L.ShepardfromJune4,1994,throughJuly1,1994.Theviolation
isassociated
withtherepeatedpackingfailuresofaUnit2mainsteamtestselectorvalveoveraperiodoftwoyearsthatresultedinseveralentriesintofour-hour
limitingconditions
ofoperation.
Ourreplytothenoticeofviolation
isprovidedintheattachment
tothisletter.Thisletterissubmitted
pursuantto10CFR50.54(f)and,assuch,anoathstatement
isattached.
p~W)VicePresident
arAttachment
940S240071
940S240071
94081PDRADDCI;05000315PDFi'gy/  
94081 PDR ADDCI;05000315 PDFi'gy/  
Mr.J.B.Martin-2-AEP:NRC:1212G
Mr.J.B.Martin-2-AEP:NRC:1212G
CC:A.A.BlindG.CharnoffW.T.Russell,NRC-Washington,
CC: A.A.Blind G.Charnoff W.T.Russell, NRC-Washington, D.C.NRC Resident Inspector NFEM Section Chief J.R.Padgett  
D.C.NRCResidentInspector
STATE OF OHIO COUNTY OF FRANKLIN E.E.Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the foregoing response to NRC INSPECTION
NFEMSectionChiefJ.R.Padgett  
REPORTS NO.50-315/94013 (DRP)AND 50-316/94013 (DRP), REPLY TO NOTICE OF VIOLATION and knows the contents thereof;and that said contents are true to the best of his knowledge and belief.Subscribed
STATEOFOHIOCOUNTYOFFRANKLINE.E.Fitzpatrick,
end sworn to before me this~PE day of 19~EX NOTARY PUBLIC Ale D.HILL gpgpy pUQUC, STAIE pF plllp SSX SSh',IEISSISS
beingdulysworn,deposesandsaysthatheistheVicePresident
oflicenseeIndianaMichiganPowerCompany,thathehasreadtheforegoing
responsetoNRCINSPECTION
REPORTSNO.50-315/94013
(DRP)AND50-316/94013
(DRP),REPLYTONOTICEOFVIOLATION
andknowsthecontentsthereof;andthatsaidcontentsaretruetothebestofhisknowledge
andbelief.Subscribed
endsworntobeforemethis~PEdayof19~EXNOTARYPUBLICAleD.HILLgpgpypUQUC,STAIEpFplllpSSXSSh',IEISSISS
EXPIRES~  
EXPIRES~  
ATTACHMENT
ATTACHMENT
TOAEP:NRC:1212G
TO AEP:NRC:1212G
REPLYTONOTICEOFVIOLATION
REPLY TO NOTICE OF VIOLATION
ATTACHMENT
ATTACHMENT
TOAEP:NRC:1212G
TO AEP:NRC:1212G
Page1Background
Page 1 Background
Aroutinesafetyinspection
A routine safety inspection
wasconducted
was conducted by Messrs.James A.Isom, David J.Hartland, and Douglas L.Shepard from Jurie 4, 1994, through July 1, 1994.During this inspection, one item was found to be in violation.
byMessrs.JamesA.Isom,DavidJ.Hartland,
The violation was identified
andDouglasL.ShepardfromJurie4,1994,throughJuly1,1994.Duringthisinspection,
as the failure to correct che root cause for the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions
oneitemwasfoundtobeinviolation.
of operation.
Theviolation
This violation was set forth in a letter containing
wasidentified
the notice of violation, dated July 20, 1994, fromMr.E.G.Greenman, Director, Division of Reactor Projects, USNRC, Region III.The letter was received July 25, 1994.Our response to the notice of violation is contained within this document.NRC Violation"10 CFR 50, Appendix B, Criterion XVI,"Corrective
asthefailuretocorrectcherootcausefortherepeatedpackingfailuresofaUnit2mainsteamtestselectorvalveoveraperiodoftwoyearsthatresultedinseveralentriesintofour-hour
Action," requires in part that"Measures shall be established
limitingconditions
to assure that conditions
ofoperation.
adverse to quality are promptly identified
Thisviolation
and corrected.
wassetforthinalettercontaining
In the case of significant
thenoticeofviolation,
datedJuly20,1994,fromMr.E.G.Greenman,
Director,
DivisionofReactorProjects,
USNRC,RegionIII.TheletterwasreceivedJuly25,1994.Ourresponsetothenoticeofviolation
iscontained
withinthisdocument.
NRCViolation
"10CFR50,AppendixB,Criterion
XVI,"Corrective
Action,"requiresinpartthat"Measures
shallbeestablished
toassurethatconditions
adversetoqualityarepromptlyidentified
andcorrected.
Inthecaseofsignificant
conditions
conditions
adversetoquality,themeasuresshallassurethatthecauseofthecondition
adverse to quality, the measures shall assure that the cause of the condition is determined
isdetermined
and corrective
andcorrective
action taken to preclude repetition." Contrary to the above, as of July 1, 1994, the licensee failed to replace the pitted valve stem on main steam stop valve (MSSV)dump valve test selector, 2-MM0-240, a significant
actiontakentoprecluderepetition."
condition adverse to quality.Specifically, Action Request 25594 had been written on July 8,'992, to replace the pitted valve stem but was not scheduled to be performed until the refueling outage starting in September 1994.Consequently, 2-MMO-240 had to be repacked five times, requiring entries into the four hour Limiting Condition of Operation (LCO), as required by Technical Specification (TS)4.7.1.5.1.
Contrarytotheabove,asofJuly1,1994,thelicenseefailedtoreplacethepittedvalvestemonmainsteamstopvalve(MSSV)dumpvalvetestselector,
There were several opportunities
2-MM0-240,
since July 1992 to replace the stem without entering the LCO.This is a Severity Level IV violation (Supplement
asignificant
condition
adversetoquality.Specifically,
ActionRequest25594hadbeenwrittenonJuly8,'992,toreplacethepittedvalvestembutwasnotscheduled
tobeperformed
untiltherefueling
outagestartinginSeptember
1994.Consequently,
2-MMO-240
hadtoberepackedfivetimes,requiring
entriesintothefourhourLimitingCondition
ofOperation
(LCO),asrequiredbyTechnical
Specification
(TS)4.7.1.5.1.
Therewereseveralopportunities
sinceJuly1992toreplacethestemwithoutenteringtheLCO.ThisisaSeverityLevelIVviolation
(Supplement
I).  
I).  
ATTACHMENT
ATTACHMENT
TOAEP:NRC:1212GPage2ResponsetoViolation
TO AEP:NRC: 1212G Page 2 Response to Violation dmissio or Denial o the Alle ed Violat o Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
dmissioorDenialotheAlleedViolatoIndianaMichiganPowerCompanyadmitstotheviolation
2.easons for the Violatio The root cause for this violation has been identified
ascitedintheNRCnoticeofviolation.
as a programmatic
2.easonsfortheViolatioTherootcauseforthisviolation
weakness in the plant's corrective
hasbeenidentified
action program.In July 1992, Unit 2 was in Mode 3 (Hot Standby).While repacking 2-MM0-240, the valve stem was found to be pitted, scored and in need of replacement.
asaprogrammatic
At that time an Action Request was initiated to replace the stem.Since a repair activity of this type requires cooldown to Mode 5 to perform, a scheduling
weaknessintheplant'scorrective
code of U2R94 was assigned, adding the repair to the scope of the 1994 refueling outage.At the time the U2R94 code was assigned, in the absence of prior failure history, this was the correct designation.
actionprogram.InJuly1992,Unit2wasinMode3(HotStandby).
The valve stem replacement
Whilerepacking
would only have been elevated to the forced outage schedule if the subsequent, repeated repairs had been identified
2-MM0-240,
as rework and an adverse trend.Since the valve stem deficiency
thevalvestemwasfoundtobepitted,scoredandinneedofreplacement.
was first identified, 2-MMO-240 has been repacked five additional
AtthattimeanActionRequestwasinitiated
times.Had the valve stem replacement
toreplacethestem.SincearepairactivityofthistyperequirescooldowntoMode5toperform,ascheduling
been scheduled as a forced outage activity, there would have been two opportunities
codeofU2R94wasassigned,
prior to the violation to complete the repair.The first opportunity
addingtherepairtothescopeofthe1994refueling
occurred in August 1993 when the unit experienced
outage.AtthetimetheU2R94codewasassigned,
a reactor trip and forced outage.The second opportunity
intheabsenceofpriorfailurehistory,thiswasthecorrectdesignation.
occurred in January 1994 when the unit was removed from service to repair an unisolable
Thevalvestemreplacement
steam leak on Steam Generator 21 blowdown line.Repeated packing replacements
wouldonlyhavebeenelevatedtotheforcedoutagescheduleifthesubsequent,
were not identified
repeatedrepairshadbeenidentified
in the plant's Corrective
asreworkandanadversetrend.Sincethevalvestemdeficiency
Action Program (PMI-7030)
wasfirstidentified,
as an adverse trend.PMI-7030,"Corrective
2-MMO-240
Action Program," requires a condition report to be written for similar corrective
hasbeenrepackedfiveadditional
times.Hadthevalvestemreplacement
beenscheduled
asaforcedoutageactivity,
therewouldhavebeentwoopportunities
priortotheviolation
tocompletetherepair.Thefirstopportunity
occurredinAugust1993whentheunitexperienced
areactortripandforcedoutage.Thesecondopportunity
occurredinJanuary1994whentheunitwasremovedfromservicetorepairanunisolable
steamleakonSteamGenerator
21blowdownline.Repeatedpackingreplacements
werenotidentified
intheplant'sCorrective
ActionProgram(PMI-7030)
asanadversetrend.PMI-7030,
"Corrective
ActionProgram,"
requiresacondition
reporttobewrittenforsimilarcorrective
maintenance
maintenance
workwithin90daysoftheoriginaldeficiency.
work within 90 days of the original deficiency.
OnlythefinalpackingfailureonMay17,1994,fellwithinthe90daycriteria,
Only the final packing failure on May 17, 1994, fell within the 90 day criteria, as this failure occurred 57 days after the previous repair on March 21, 1994.  
asthisfailureoccurred57daysafterthepreviousrepaironMarch21,1994.  
ATTACHMENT
ATTACHMENT
TOAEP:NRC:12120Page3Areworkcondition
TO AEP:NRC: 12120 Page 3 A rework condition report was not initiated following the May 17 failure due to an error in the Maintenance
reportwasnotinitiated
following
theMay17failureduetoanerrorintheMaintenance
Administrative
Administrative
Procedure
Procedure (MAP)¹MA3.3-05,"Maintenance
(MAP)¹MA3.3-05,
"Maintenance
Planning".
Planning".
MAP¹MA3.3-05
MAP¹MA3.3-05 incorrectly
incorrectly
defined rework as similar work performed within 30 days of the original failure, rather than 90 days.As a result of this error the maintenance
definedreworkassimilarworkperformed
planner failed to identify the reoccurrence
within30daysoftheoriginalfailure,ratherthan90days.Asaresultofthiserrorthemaintenance
of the packing leak on May 17, 1994, as falling within the definition
plannerfailedtoidentifythereoccurrence
of rework.3.Cor ective Actions Taken and esults eyed The work control process code was changed on the 2-MMO-240 repair Job Order.The 2-MMO-240 repair task now appears on the forced outage schedule, as well as within the scope of the refueling outage.MAP¹MA3.3-05,"Maintenance
ofthepackingleakonMay17,1994,asfallingwithinthedefinition
Planning," was revised to reflect the current definition
ofrework.3.CorectiveActionsTakenandesultseyedTheworkcontrolprocesscodewaschangedonthe2-MMO-240
of rework contained in PMI-7030.4.Corrective
repairJobOrder.The2-MMO-240
Actions Taken to Avoid Further Violations
repairtasknowappearsontheforcedoutageschedule,
PMI-7030,"Corrective
aswellaswithinthescopeoftherefueling
Action," will be revised to redefine rework.The definition
outage.MAP¹MA3.3-05,
for rework will now include any corrective
"Maintenance
Planning,"
wasrevisedtoreflectthecurrentdefinition
ofreworkcontained
inPMI-7030.4.Corrective
ActionsTakentoAvoidFurtherViolations
PMI-7030,
"Corrective
Action,"willberevisedtoredefinerework.Thedefinition
forreworkwillnowincludeanycorrective
maintenance
maintenance
whichrequiresentryintoaLimitingCondition
which requires entry into a Limiting Condition of Operation (LCO)if similar work has been performed on that equipment/component
ofOperation
during the current operating cycle, including the previous refueling outage.When rework of this type occurs, a Condition Report will be written to aid in the identification/evaluation
(LCO)ifsimilarworkhasbeenperformed
of an adverse trend.The"90-day" standard will be retained for work upon equipment or components
onthatequipment/component
which do not initiate an LCO entry.MAP¹MA3.3-05,"Maintenance
duringthecurrentoperating
Planning," will be revised to refer to PMI-7030 for the above-described
cycle,including
thepreviousrefueling
outage.Whenreworkofthistypeoccurs,aCondition
Reportwillbewrittentoaidintheidentification/evaluation
ofanadversetrend.The"90-day"standardwillberetainedforworkuponequipment
orcomponents
whichdonotinitiateanLCOentry.MAP¹MA3.3-05,
"Maintenance
Planning,"
willberevisedtorefertoPMI-7030fortheabove-described
redefinition
redefinition
ofrework.Thesemeasureswillassurethatthistypeofcondition
of rework.These measures will assure that this type of condition will be precluded in the future.5.ate When Full Com lienee Will Be Achieved PMI-7030 and MAP modifications
willbeprecluded
will be completed by September 30, 1994.  
inthefuture.5.ateWhenFullComlieneeWillBeAchievedPMI-7030andMAPmodifications
willbecompleted
bySeptember
30,1994.  
ATTACHMENT
ATTACHMENT
TOAEP:NRC:1212G
TO AEP:NRC:1212G
Page4Thevalvestemreplacement
Page 4 The valve stem replacement
for2-MMO-240
for 2-MMO-240 will be completed during the first Mode 5 forced outage of sufficient
willbecompleted
duration or the upcoming Unit 2 refueling outage, scheduled to commence September 6, 1994, whichever occurs first.
duringthefirstMode5forcedoutageofsufficient
durationortheupcomingUnit2refueling
outage,scheduled
tocommenceSeptember
6,1994,whichever
occursfirst.
}}
}}

Revision as of 07:17, 6 July 2018

Responds to NRC 940720 Ltr Re Violation Noted in Insp Repts 50-315/94-13 & 50-316/94-13.Corrective Actions:Work Control Process Code Was Changed on 2-MMO-240 Repair Job Order & CAP PMI-7030 Will Be Revised to Redefine Rework
ML17332A260
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 08/19/1994
From: FITZPATRICK E
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: MARTIN J B
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1212G, NUDOCS 9408240071
Download: ML17332A260 (10)


See also: IR 05000315/1994013

Text

(ACCELERATED

RIDS PROCESSING)

R EGULATORY INFORMATION

DISTRIBUTION

SYSTEM (RIDS)'CESSION NBR:9408240071

DOC.DATE: 94/08/19 NOTARIZED:

YES DOCKET FACIL:50-315

Donald C.Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C.Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH.NAME AUTHOR AFFILIATION

FITZPATRICK,E.

Indiana Michigan Power Co.(formerly Indiana&Michigan Ele RECIP.NAME

RECIPIENT AFFILIATION

Document Control Branch (Document Control Desk)SUBJECT: Responds to NRC 940720 ltr re violations

noted in insp rept 50-315/94-13

&50-316/94-13.Corrective

actions:work

control process code was changed on 2-MMO-240 repair job order&PMI-7030 will be revised to redefine rework.DISTRIBUTION

CODE: IE01D COPIES RECEIVED:LTR

ENCL SIZE: TITLE: General (50 Dkt)-Insp Rept/Notice

of Vio ation Response NOTES: RECIPIENT ID CODE/NAME PD3-1 PD INTERNAL: AEOD/DE I B AEOD/S PD/RRAB DEDRO NRR/DRCH/HHFB, NUDOCS-ABSTRACT

OGC/HDS2 RES/HFB EXTERNAL EG&G/BRYCE i J~H~NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME HICKMAN,J AEOD/SPD/RAB

AEOD/TTC NRR/DORS/OEAB

NRR/PMAS/IRCB-E

0 R REG FIL 02 GN3 FILE 01 NOAC COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 NOTE TO ALL"RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE iVASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.504-2083)TO ELIMINATE YOUR NAME F ROTI DISTRIBUTION

LISTS FOR DOCUMENTS YOU DON"I'EED!TOTAL NUMBER OF COPIES REQUIRED'TTR

19 ENCL 19

Indiana Michigan Power Company P.O.Box 16631 Columbus, OH 43216 INDIANA NICHIGAN POWER AEP;NRC'1212G

10 CFR 2.201 Donald C.Cook Nuclear Plant Units 1 and 2 Docket Nos.50-315 and 50-316 License Nos.DPR-58 and DPR-74 NRC INSPECTION

REPORTS NO.50-315/94013 (DRP)AND 50-316/94013 (DRP)REPLY TO NOTICE OF VIOLATION U.S.Nuclear Regulatory

Commission

Document Control Desk Washington, D.C.20555 Attn: Mr.J.B.Martin August 19, 1994 Dear Mr.Martin: This letter is in response to a USNRC letter dated July 20, 1994, that forwarded a notice of violation to Indiana Michigan Power Company.The notice of violation contained one violation identified

during a routine safety inspection

conducted by Messrs.J.A.Isom, D.J.Hartland, and D.L.Shepard from June 4, 1994, through July 1, 1994.The violation is associated

with the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions

of operation.

Our reply to the notice of violation is provided in the attachment

to this letter.This letter is submitted pursuant to 10 CFR 50.54(f)and, as such, an oath statement is attached.p~W)Vice President ar Attachment

940S240071

94081 PDR ADDCI;05000315 PDFi'gy/

Mr.J.B.Martin-2-AEP:NRC:1212G

CC: A.A.Blind G.Charnoff W.T.Russell, NRC-Washington, D.C.NRC Resident Inspector NFEM Section Chief J.R.Padgett

STATE OF OHIO COUNTY OF FRANKLIN E.E.Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the foregoing response to NRC INSPECTION

REPORTS NO.50-315/94013 (DRP)AND 50-316/94013 (DRP), REPLY TO NOTICE OF VIOLATION and knows the contents thereof;and that said contents are true to the best of his knowledge and belief.Subscribed

end sworn to before me this~PE day of 19~EX NOTARY PUBLIC Ale D.HILL gpgpy pUQUC, STAIE pF plllp SSX SSh',IEISSISS

EXPIRES~

ATTACHMENT

TO AEP:NRC:1212G

REPLY TO NOTICE OF VIOLATION

ATTACHMENT

TO AEP:NRC:1212G

Page 1 Background

A routine safety inspection

was conducted by Messrs.James A.Isom, David J.Hartland, and Douglas L.Shepard from Jurie 4, 1994, through July 1, 1994.During this inspection, one item was found to be in violation.

The violation was identified

as the failure to correct che root cause for the repeated packing failures of a Unit 2 main steam test selector valve over a period of two years that resulted in several entries into four-hour limiting conditions

of operation.

This violation was set forth in a letter containing

the notice of violation, dated July 20, 1994, fromMr.E.G.Greenman, Director, Division of Reactor Projects, USNRC, Region III.The letter was received July 25, 1994.Our response to the notice of violation is contained within this document.NRC Violation"10 CFR 50, Appendix B, Criterion XVI,"Corrective

Action," requires in part that"Measures shall be established

to assure that conditions

adverse to quality are promptly identified

and corrected.

In the case of significant

conditions

adverse to quality, the measures shall assure that the cause of the condition is determined

and corrective

action taken to preclude repetition." Contrary to the above, as of July 1, 1994, the licensee failed to replace the pitted valve stem on main steam stop valve (MSSV)dump valve test selector, 2-MM0-240, a significant

condition adverse to quality.Specifically, Action Request 25594 had been written on July 8,'992, to replace the pitted valve stem but was not scheduled to be performed until the refueling outage starting in September 1994.Consequently, 2-MMO-240 had to be repacked five times, requiring entries into the four hour Limiting Condition of Operation (LCO), as required by Technical Specification (TS)4.7.1.5.1.

There were several opportunities

since July 1992 to replace the stem without entering the LCO.This is a Severity Level IV violation (Supplement

I).

ATTACHMENT

TO AEP:NRC: 1212G Page 2 Response to Violation dmissio or Denial o the Alle ed Violat o Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.

2.easons for the Violatio The root cause for this violation has been identified

as a programmatic

weakness in the plant's corrective

action program.In July 1992, Unit 2 was in Mode 3 (Hot Standby).While repacking 2-MM0-240, the valve stem was found to be pitted, scored and in need of replacement.

At that time an Action Request was initiated to replace the stem.Since a repair activity of this type requires cooldown to Mode 5 to perform, a scheduling

code of U2R94 was assigned, adding the repair to the scope of the 1994 refueling outage.At the time the U2R94 code was assigned, in the absence of prior failure history, this was the correct designation.

The valve stem replacement

would only have been elevated to the forced outage schedule if the subsequent, repeated repairs had been identified

as rework and an adverse trend.Since the valve stem deficiency

was first identified, 2-MMO-240 has been repacked five additional

times.Had the valve stem replacement

been scheduled as a forced outage activity, there would have been two opportunities

prior to the violation to complete the repair.The first opportunity

occurred in August 1993 when the unit experienced

a reactor trip and forced outage.The second opportunity

occurred in January 1994 when the unit was removed from service to repair an unisolable

steam leak on Steam Generator 21 blowdown line.Repeated packing replacements

were not identified

in the plant's Corrective

Action Program (PMI-7030)

as an adverse trend.PMI-7030,"Corrective

Action Program," requires a condition report to be written for similar corrective

maintenance

work within 90 days of the original deficiency.

Only the final packing failure on May 17, 1994, fell within the 90 day criteria, as this failure occurred 57 days after the previous repair on March 21, 1994.

ATTACHMENT

TO AEP:NRC: 12120 Page 3 A rework condition report was not initiated following the May 17 failure due to an error in the Maintenance

Administrative

Procedure (MAP)¹MA3.3-05,"Maintenance

Planning".

MAP¹MA3.3-05 incorrectly

defined rework as similar work performed within 30 days of the original failure, rather than 90 days.As a result of this error the maintenance

planner failed to identify the reoccurrence

of the packing leak on May 17, 1994, as falling within the definition

of rework.3.Cor ective Actions Taken and esults eyed The work control process code was changed on the 2-MMO-240 repair Job Order.The 2-MMO-240 repair task now appears on the forced outage schedule, as well as within the scope of the refueling outage.MAP¹MA3.3-05,"Maintenance

Planning," was revised to reflect the current definition

of rework contained in PMI-7030.4.Corrective

Actions Taken to Avoid Further Violations

PMI-7030,"Corrective

Action," will be revised to redefine rework.The definition

for rework will now include any corrective

maintenance

which requires entry into a Limiting Condition of Operation (LCO)if similar work has been performed on that equipment/component

during the current operating cycle, including the previous refueling outage.When rework of this type occurs, a Condition Report will be written to aid in the identification/evaluation

of an adverse trend.The"90-day" standard will be retained for work upon equipment or components

which do not initiate an LCO entry.MAP¹MA3.3-05,"Maintenance

Planning," will be revised to refer to PMI-7030 for the above-described

redefinition

of rework.These measures will assure that this type of condition will be precluded in the future.5.ate When Full Com lienee Will Be Achieved PMI-7030 and MAP modifications

will be completed by September 30, 1994.

ATTACHMENT

TO AEP:NRC:1212G

Page 4 The valve stem replacement

for 2-MMO-240 will be completed during the first Mode 5 forced outage of sufficient

duration or the upcoming Unit 2 refueling outage, scheduled to commence September 6, 1994, whichever occurs first.