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{{#Wiki_filter:(ACCELERATEDRIDSPROCESSING)REGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)'CESSIONNBR:9408240071DOC.DATE:94/08/19NOTARIZED:YESDOCKETFACIL:50-315DonaldC.CookNuclearPowerPlant,Unit1,IndianaM0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,IndianaM05000316AUTH.NAMEAUTHORAFFILIATIONFITZPATRICK,E.IndianaMichiganPowerCo.(formerlyIndiana&MichiganEleRECIP.NAMERECIPIENTAFFILIATIONDocumentControlBranch(DocumentControlDesk)SUBJECT:RespondstoNRC940720ltrreviolationsnotedininsprept50-315/94-13&50-316/94-13.Correctiveactions:workcontrolprocesscodewaschangedon2-MMO-240repairjoborder&PMI-7030willberevisedtoredefinerework.DISTRIBUTIONCODE:IE01DCOPIESRECEIVED:LTRENCLSIZE:TITLE:General(50Dkt)-InspRept/NoticeofVioationResponseNOTES:RECIPIENTIDCODE/NAMEPD3-1PDINTERNAL:AEOD/DEIBAEOD/SPD/RRABDEDRONRR/DRCH/HHFB,NUDOCS-ABSTRACTOGC/HDS2RES/HFBEXTERNALEG&G/BRYCEiJ~H~NRCPDRCOPIESLTTRENCL11111111111111111111RECIPIENTIDCODE/NAMEHICKMAN,JAEOD/SPD/RABAEOD/TTCNRR/DORS/OEABNRR/PMAS/IRCB-E0RREGFIL02GN3FILE01NOACCOPIESLTTRENCL111111111111111111NOTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEiVASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2083)TOELIMINATEYOURNAMEFROTIDISTRIBUTIONLISTSFORDOCUMENTSYOUDON"I'EED!TOTALNUMBEROFCOPIESREQUIRED'TTR19ENCL19
{{#Wiki_filter:(ACCELERATED
RIDSPROCESSING)
REGULATORY
INFORMATION
DISTRIBUTION
SYSTEM(RIDS)'CESSIONNBR:9408240071
DOC.DATE:
94/08/19NOTARIZED:
YESDOCKETFACIL:50-315
DonaldC.CookNuclearPowerPlant,Unit1,IndianaM0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,IndianaM05000316AUTH.NAMEAUTHORAFFILIATION
FITZPATRICK,E.
IndianaMichiganPowerCo.(formerly
Indiana&MichiganEleRECIP.NAME
RECIPIENT
AFFILIATION
DocumentControlBranch(Document
ControlDesk)SUBJECT:RespondstoNRC940720ltrreviolations
notedininsprept50-315/94-13
&50-316/94-13.Corrective
actions:work
controlprocesscodewaschangedon2-MMO-240
repairjoborder&PMI-7030willberevisedtoredefinerework.DISTRIBUTION
CODE:IE01DCOPIESRECEIVED:LTR
ENCLSIZE:TITLE:General(50Dkt)-Insp
Rept/Notice
ofVioationResponseNOTES:RECIPIENT
IDCODE/NAME
PD3-1PDINTERNAL:
AEOD/DEIBAEOD/SPD/RRABDEDRONRR/DRCH/HHFB,
NUDOCS-ABSTRACT
OGC/HDS2RES/HFBEXTERNALEG&G/BRYCEiJ~H~NRCPDRCOPIESLTTRENCL11111111111111111111RECIPIENT
IDCODE/NAME
HICKMAN,J
AEOD/SPD/RAB
AEOD/TTCNRR/DORS/OEAB
NRR/PMAS/IRCB-E
0RREGFIL02GN3FILE01NOACCOPIESLTTRENCL111111111111111111NOTETOALL"RIDS"RECIPIENTS:
PLEASEHELPUSTOREDUCEiVASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2083)TOELIMINATE
YOURNAMEFROTIDISTRIBUTION
LISTSFORDOCUMENTS
YOUDON"I'EED!TOTALNUMBEROFCOPIESREQUIRED'TTR
19ENCL19
   
   
IndianaMichiganPowerCompanyP.O.Box16631Columbus,OH43216INDIANANICHIGANPOWERAEP;NRC'1212G10CFR2.201DonaldC.CookNuclearPlantUnits1and2DocketNos.50-315and50-316LicenseNos.DPR-58andDPR-74NRCINSPECTIONREPORTSNO.50-315/94013(DRP)AND50-316/94013(DRP)REPLYTONOTICEOFVIOLATIONU.S.NuclearRegulatoryCommissionDocumentControlDeskWashington,D.C.20555Attn:Mr.J.B.MartinAugust19,1994DearMr.Martin:ThisletterisinresponsetoaUSNRCletterdatedJuly20,1994,thatforwardedanoticeofviolationtoIndianaMichiganPowerCompany.ThenoticeofviolationcontainedoneviolationidentifiedduringaroutinesafetyinspectionconductedbyMessrs.J.A.Isom,D.J.Hartland,andD.L.ShepardfromJune4,1994,throughJuly1,1994.TheviolationisassociatedwiththerepeatedpackingfailuresofaUnit2mainsteamtestselectorvalveoveraperiodoftwoyearsthatresultedinseveralentriesintofour-hourlimitingconditionsofoperation.Ourreplytothenoticeofviolationisprovidedintheattachmenttothisletter.Thisletterissubmittedpursuantto10CFR50.54(f)and,assuch,anoathstatementisattached.p~W)VicePresidentarAttachment940S24007194081PDRADDCI;05000315PDFi'gy/  
IndianaMichiganPowerCompanyP.O.Box16631Columbus,
Mr.J.B.Martin-2-AEP:NRC:1212GCC:A.A.BlindG.CharnoffW.T.Russell,NRC-Washington,D.C.NRCResidentInspectorNFEMSectionChiefJ.R.Padgett  
OH43216INDIANANICHIGANPOWERAEP;NRC'1212G
STATEOFOHIOCOUNTYOFFRANKLINE.E.Fitzpatrick,beingdulysworn,deposesandsaysthatheistheVicePresidentoflicenseeIndianaMichiganPowerCompany,thathehasreadtheforegoingresponsetoNRCINSPECTIONREPORTSNO.50-315/94013(DRP)AND50-316/94013(DRP),REPLYTONOTICEOFVIOLATIONandknowsthecontentsthereof;andthatsaidcontentsaretruetothebestofhisknowledgeandbelief.Subscribedendsworntobeforemethis~PEdayof19~EXNOTARYPUBLICAleD.HILLgpgpypUQUC,STAIEpFplllpSSXSSh',IEISSISSEXPIRES~  
10CFR2.201DonaldC.CookNuclearPlantUnits1and2DocketNos.50-315and50-316LicenseNos.DPR-58andDPR-74NRCINSPECTION
ATTACHMENTTOAEP:NRC:1212GREPLYTONOTICEOFVIOLATION
REPORTSNO.50-315/94013
ATTACHMENTTOAEP:NRC:1212GPage1BackgroundAroutinesafetyinspectionwasconductedbyMessrs.JamesA.Isom,DavidJ.Hartland,andDouglasL.ShepardfromJurie4,1994,throughJuly1,1994.Duringthisinspection,oneitemwasfoundtobeinviolation.TheviolationwasidentifiedasthefailuretocorrectcherootcausefortherepeatedpackingfailuresofaUnit2mainsteamtestselectorvalveoveraperiodoftwoyearsthatresultedinseveralentriesintofour-hourlimitingconditionsofoperation.Thisviolationwassetforthinalettercontainingthenoticeofviolation,datedJuly20,1994,fromMr.E.G.Greenman,Director,DivisionofReactorProjects,USNRC,RegionIII.TheletterwasreceivedJuly25,1994.Ourresponsetothenoticeofviolationiscontainedwithinthisdocument.NRCViolation"10CFR50,AppendixB,CriterionXVI,"CorrectiveAction,"requiresinpartthat"Measuresshallbeestablishedtoassurethatconditionsadversetoqualityarepromptlyidentifiedandcorrected.Inthecaseofsignificantconditionsadversetoquality,themeasuresshallassurethatthecauseoftheconditionisdeterminedandcorrectiveactiontakentoprecluderepetition."Contrarytotheabove,asofJuly1,1994,thelicenseefailedtoreplacethepittedvalvestemonmainsteamstopvalve(MSSV)dumpvalvetestselector,2-MM0-240,asignificantconditionadversetoquality.Specifically,ActionRequest25594hadbeenwrittenonJuly8,'992,toreplacethepittedvalvestembutwasnotscheduledtobeperformeduntiltherefuelingoutagestartinginSeptember1994.Consequently,2-MMO-240hadtoberepackedfivetimes,requiringentriesintothefourhourLimitingConditionofOperation(LCO),asrequiredbyTechnicalSpecification(TS)4.7.1.5.1.TherewereseveralopportunitiessinceJuly1992toreplacethestemwithoutenteringtheLCO.ThisisaSeverityLevelIVviolation(SupplementI).  
(DRP)AND50-316/94013
ATTACHMENTTOAEP:NRC:1212GPage2ResponsetoViolationdmissioorDenialotheAlleedViolatoIndianaMichiganPowerCompanyadmitstotheviolationascitedintheNRCnoticeofviolation.2.easonsfortheViolatioTherootcauseforthisviolationhasbeenidentifiedasaprogrammaticweaknessintheplant'scorrectiveactionprogram.InJuly1992,Unit2wasinMode3(HotStandby).Whilerepacking2-MM0-240,thevalvestemwasfoundtobepitted,scoredandinneedofreplacement.AtthattimeanActionRequestwasinitiatedtoreplacethestem.SincearepairactivityofthistyperequirescooldowntoMode5toperform,aschedulingcodeofU2R94wasassigned,addingtherepairtothescopeofthe1994refuelingoutage.AtthetimetheU2R94codewasassigned,intheabsenceofpriorfailurehistory,thiswasthecorrectdesignation.Thevalvestemreplacementwouldonlyhavebeenelevatedtotheforcedoutagescheduleifthesubsequent,repeatedrepairshadbeenidentifiedasreworkandanadversetrend.Sincethevalvestemdeficiencywasfirstidentified,2-MMO-240hasbeenrepackedfiveadditionaltimes.Hadthevalvestemreplacementbeenscheduledasaforcedoutageactivity,therewouldhavebeentwoopportunitiespriortotheviolationtocompletetherepair.ThefirstopportunityoccurredinAugust1993whentheunitexperiencedareactortripandforcedoutage.ThesecondopportunityoccurredinJanuary1994whentheunitwasremovedfromservicetorepairanunisolablesteamleakonSteamGenerator21blowdownline.Repeatedpackingreplacementswerenotidentifiedintheplant'sCorrectiveActionProgram(PMI-7030)asanadversetrend.PMI-7030,"CorrectiveActionProgram,"requiresaconditionreporttobewrittenforsimilarcorrectivemaintenanceworkwithin90daysoftheoriginaldeficiency.OnlythefinalpackingfailureonMay17,1994,fellwithinthe90daycriteria,asthisfailureoccurred57daysafterthepreviousrepaironMarch21,1994.  
(DRP)REPLYTONOTICEOFVIOLATION
ATTACHMENTTOAEP:NRC:12120Page3AreworkconditionreportwasnotinitiatedfollowingtheMay17failureduetoanerrorintheMaintenanceAdministrativeProcedure(MAP)¹MA3.3-05,"MaintenancePlanning".MAP¹MA3.3-05incorrectlydefinedreworkassimilarworkperformedwithin30daysoftheoriginalfailure,ratherthan90days.AsaresultofthiserrorthemaintenanceplannerfailedtoidentifythereoccurrenceofthepackingleakonMay17,1994,asfallingwithinthedefinitionofrework.3.CorectiveActionsTakenandesultseyedTheworkcontrolprocesscodewaschangedonthe2-MMO-240repairJobOrder.The2-MMO-240repairtasknowappearsontheforcedoutageschedule,aswellaswithinthescopeoftherefuelingoutage.MAP¹MA3.3-05,"MaintenancePlanning,"wasrevisedtoreflectthecurrentdefinitionofreworkcontainedinPMI-7030.4.CorrectiveActionsTakentoAvoidFurtherViolationsPMI-7030,"CorrectiveAction,"willberevisedtoredefinerework.ThedefinitionforreworkwillnowincludeanycorrectivemaintenancewhichrequiresentryintoaLimitingConditionofOperation(LCO)ifsimilarworkhasbeenperformedonthatequipment/componentduringthecurrentoperatingcycle,includingthepreviousrefuelingoutage.Whenreworkofthistypeoccurs,aConditionReportwillbewrittentoaidintheidentification/evaluationofanadversetrend.The"90-day"standardwillberetainedforworkuponequipmentorcomponentswhichdonotinitiateanLCOentry.MAP¹MA3.3-05,"MaintenancePlanning,"willberevisedtorefertoPMI-7030fortheabove-describedredefinitionofrework.Thesemeasureswillassurethatthistypeofconditionwillbeprecludedinthefuture.5.ateWhenFullComlieneeWillBeAchievedPMI-7030andMAPmodificationswillbecompletedbySeptember30,1994.  
U.S.NuclearRegulatory
ATTACHMENTTOAEP:NRC:1212GPage4Thevalvestemreplacementfor2-MMO-240willbecompletedduringthefirstMode5forcedoutageofsufficientdurationortheupcomingUnit2refuelingoutage,scheduledtocommenceSeptember6,1994,whicheveroccursfirst.
Commission
DocumentControlDeskWashington,
D.C.20555Attn:Mr.J.B.MartinAugust19,1994DearMr.Martin:ThisletterisinresponsetoaUSNRCletterdatedJuly20,1994,thatforwarded
anoticeofviolation
toIndianaMichiganPowerCompany.Thenoticeofviolation
contained
oneviolation
identified
duringaroutinesafetyinspection
conducted
byMessrs.J.A.Isom,D.J.Hartland,
andD.L.ShepardfromJune4,1994,throughJuly1,1994.Theviolation
isassociated
withtherepeatedpackingfailuresofaUnit2mainsteamtestselectorvalveoveraperiodoftwoyearsthatresultedinseveralentriesintofour-hour
limitingconditions
ofoperation.
Ourreplytothenoticeofviolation
isprovidedintheattachment
tothisletter.Thisletterissubmitted
pursuantto10CFR50.54(f)and,assuch,anoathstatement
isattached.
p~W)VicePresident
arAttachment
940S240071
94081PDRADDCI;05000315PDFi'gy/  
Mr.J.B.Martin-2-AEP:NRC:1212G
CC:A.A.BlindG.CharnoffW.T.Russell,NRC-Washington,
D.C.NRCResidentInspector
NFEMSectionChiefJ.R.Padgett  
STATEOFOHIOCOUNTYOFFRANKLINE.E.Fitzpatrick,
beingdulysworn,deposesandsaysthatheistheVicePresident
oflicenseeIndianaMichiganPowerCompany,thathehasreadtheforegoing
responsetoNRCINSPECTION
REPORTSNO.50-315/94013
(DRP)AND50-316/94013
(DRP),REPLYTONOTICEOFVIOLATION
andknowsthecontentsthereof;andthatsaidcontentsaretruetothebestofhisknowledge
andbelief.Subscribed
endsworntobeforemethis~PEdayof19~EXNOTARYPUBLICAleD.HILLgpgpypUQUC,STAIEpFplllpSSXSSh',IEISSISS
EXPIRES~  
ATTACHMENT
TOAEP:NRC:1212G
REPLYTONOTICEOFVIOLATION
ATTACHMENT
TOAEP:NRC:1212G
Page1Background
Aroutinesafetyinspection
wasconducted
byMessrs.JamesA.Isom,DavidJ.Hartland,
andDouglasL.ShepardfromJurie4,1994,throughJuly1,1994.Duringthisinspection,
oneitemwasfoundtobeinviolation.
Theviolation
wasidentified
asthefailuretocorrectcherootcausefortherepeatedpackingfailuresofaUnit2mainsteamtestselectorvalveoveraperiodoftwoyearsthatresultedinseveralentriesintofour-hour
limitingconditions
ofoperation.
Thisviolation
wassetforthinalettercontaining
thenoticeofviolation,
datedJuly20,1994,fromMr.E.G.Greenman,
Director,
DivisionofReactorProjects,
USNRC,RegionIII.TheletterwasreceivedJuly25,1994.Ourresponsetothenoticeofviolation
iscontained
withinthisdocument.
NRCViolation
"10CFR50,AppendixB,Criterion
XVI,"Corrective
Action,"requiresinpartthat"Measures
shallbeestablished
toassurethatconditions
adversetoqualityarepromptlyidentified
andcorrected.
Inthecaseofsignificant
conditions
adversetoquality,themeasuresshallassurethatthecauseofthecondition
isdetermined
andcorrective
actiontakentoprecluderepetition."
Contrarytotheabove,asofJuly1,1994,thelicenseefailedtoreplacethepittedvalvestemonmainsteamstopvalve(MSSV)dumpvalvetestselector,
2-MM0-240,
asignificant
condition
adversetoquality.Specifically,
ActionRequest25594hadbeenwrittenonJuly8,'992,toreplacethepittedvalvestembutwasnotscheduled
tobeperformed
untiltherefueling
outagestartinginSeptember
1994.Consequently,
2-MMO-240
hadtoberepackedfivetimes,requiring
entriesintothefourhourLimitingCondition
ofOperation
(LCO),asrequiredbyTechnical
Specification
(TS)4.7.1.5.1.
Therewereseveralopportunities
sinceJuly1992toreplacethestemwithoutenteringtheLCO.ThisisaSeverityLevelIVviolation
(Supplement
I).  
ATTACHMENT
TOAEP:NRC:1212GPage2ResponsetoViolation
dmissioorDenialotheAlleedViolatoIndianaMichiganPowerCompanyadmitstotheviolation
ascitedintheNRCnoticeofviolation.
2.easonsfortheViolatioTherootcauseforthisviolation
hasbeenidentified
asaprogrammatic
weaknessintheplant'scorrective
actionprogram.InJuly1992,Unit2wasinMode3(HotStandby).
Whilerepacking
2-MM0-240,
thevalvestemwasfoundtobepitted,scoredandinneedofreplacement.
AtthattimeanActionRequestwasinitiated
toreplacethestem.SincearepairactivityofthistyperequirescooldowntoMode5toperform,ascheduling
codeofU2R94wasassigned,
addingtherepairtothescopeofthe1994refueling
outage.AtthetimetheU2R94codewasassigned,
intheabsenceofpriorfailurehistory,thiswasthecorrectdesignation.
Thevalvestemreplacement
wouldonlyhavebeenelevatedtotheforcedoutagescheduleifthesubsequent,
repeatedrepairshadbeenidentified
asreworkandanadversetrend.Sincethevalvestemdeficiency
wasfirstidentified,
2-MMO-240
hasbeenrepackedfiveadditional
times.Hadthevalvestemreplacement
beenscheduled
asaforcedoutageactivity,
therewouldhavebeentwoopportunities
priortotheviolation
tocompletetherepair.Thefirstopportunity
occurredinAugust1993whentheunitexperienced
areactortripandforcedoutage.Thesecondopportunity
occurredinJanuary1994whentheunitwasremovedfromservicetorepairanunisolable
steamleakonSteamGenerator
21blowdownline.Repeatedpackingreplacements
werenotidentified
intheplant'sCorrective
ActionProgram(PMI-7030)
asanadversetrend.PMI-7030,
"Corrective
ActionProgram,"
requiresacondition
reporttobewrittenforsimilarcorrective
maintenance
workwithin90daysoftheoriginaldeficiency.
OnlythefinalpackingfailureonMay17,1994,fellwithinthe90daycriteria,
asthisfailureoccurred57daysafterthepreviousrepaironMarch21,1994.  
ATTACHMENT
TOAEP:NRC:12120Page3Areworkcondition
reportwasnotinitiated
following
theMay17failureduetoanerrorintheMaintenance
Administrative
Procedure
(MAP)¹MA3.3-05,
"Maintenance
Planning".
MAP¹MA3.3-05
incorrectly
definedreworkassimilarworkperformed
within30daysoftheoriginalfailure,ratherthan90days.Asaresultofthiserrorthemaintenance
plannerfailedtoidentifythereoccurrence
ofthepackingleakonMay17,1994,asfallingwithinthedefinition
ofrework.3.CorectiveActionsTakenandesultseyedTheworkcontrolprocesscodewaschangedonthe2-MMO-240
repairJobOrder.The2-MMO-240
repairtasknowappearsontheforcedoutageschedule,
aswellaswithinthescopeoftherefueling
outage.MAP¹MA3.3-05,
"Maintenance
Planning,"
wasrevisedtoreflectthecurrentdefinition
ofreworkcontained
inPMI-7030.4.Corrective
ActionsTakentoAvoidFurtherViolations
PMI-7030,
"Corrective
Action,"willberevisedtoredefinerework.Thedefinition
forreworkwillnowincludeanycorrective
maintenance
whichrequiresentryintoaLimitingCondition
ofOperation
(LCO)ifsimilarworkhasbeenperformed
onthatequipment/component
duringthecurrentoperating
cycle,including
thepreviousrefueling
outage.Whenreworkofthistypeoccurs,aCondition
Reportwillbewrittentoaidintheidentification/evaluation
ofanadversetrend.The"90-day"standardwillberetainedforworkuponequipment
orcomponents
whichdonotinitiateanLCOentry.MAP¹MA3.3-05,
"Maintenance
Planning,"
willberevisedtorefertoPMI-7030fortheabove-described
redefinition
ofrework.Thesemeasureswillassurethatthistypeofcondition
willbeprecluded
inthefuture.5.ateWhenFullComlieneeWillBeAchievedPMI-7030andMAPmodifications
willbecompleted
bySeptember
30,1994.  
ATTACHMENT
TOAEP:NRC:1212G
Page4Thevalvestemreplacement
for2-MMO-240
willbecompleted
duringthefirstMode5forcedoutageofsufficient
durationortheupcomingUnit2refueling
outage,scheduled
tocommenceSeptember
6,1994,whichever
occursfirst.
}}
}}

Revision as of 07:08, 29 June 2018

Responds to NRC 940720 Ltr Re Violation Noted in Insp Repts 50-315/94-13 & 50-316/94-13.Corrective Actions:Work Control Process Code Was Changed on 2-MMO-240 Repair Job Order & CAP PMI-7030 Will Be Revised to Redefine Rework
ML17332A260
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 08/19/1994
From: FITZPATRICK E
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: MARTIN J B
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1212G, NUDOCS 9408240071
Download: ML17332A260 (10)


See also: IR 05000315/1994013

Text

(ACCELERATED

RIDSPROCESSING)

REGULATORY

INFORMATION

DISTRIBUTION

SYSTEM(RIDS)'CESSIONNBR:9408240071

DOC.DATE:

94/08/19NOTARIZED:

YESDOCKETFACIL:50-315

DonaldC.CookNuclearPowerPlant,Unit1,IndianaM0500031550-316DonaldC.CookNuclearPowerPlant,Unit2,IndianaM05000316AUTH.NAMEAUTHORAFFILIATION

FITZPATRICK,E.

IndianaMichiganPowerCo.(formerly

Indiana&MichiganEleRECIP.NAME

RECIPIENT

AFFILIATION

DocumentControlBranch(Document

ControlDesk)SUBJECT:RespondstoNRC940720ltrreviolations

notedininsprept50-315/94-13

&50-316/94-13.Corrective

actions:work

controlprocesscodewaschangedon2-MMO-240

repairjoborder&PMI-7030willberevisedtoredefinerework.DISTRIBUTION

CODE:IE01DCOPIESRECEIVED:LTR

ENCLSIZE:TITLE:General(50Dkt)-Insp

Rept/Notice

ofVioationResponseNOTES:RECIPIENT

IDCODE/NAME

PD3-1PDINTERNAL:

AEOD/DEIBAEOD/SPD/RRABDEDRONRR/DRCH/HHFB,

NUDOCS-ABSTRACT

OGC/HDS2RES/HFBEXTERNALEG&G/BRYCEiJ~H~NRCPDRCOPIESLTTRENCL11111111111111111111RECIPIENT

IDCODE/NAME

HICKMAN,J

AEOD/SPD/RAB

AEOD/TTCNRR/DORS/OEAB

NRR/PMAS/IRCB-E

0RREGFIL02GN3FILE01NOACCOPIESLTTRENCL111111111111111111NOTETOALL"RIDS"RECIPIENTS:

PLEASEHELPUSTOREDUCEiVASTE!CONTACTTHEDOCUMENTCONTROLDESK,ROOMPl-37(EXT.504-2083)TOELIMINATE

YOURNAMEFROTIDISTRIBUTION

LISTSFORDOCUMENTS

YOUDON"I'EED!TOTALNUMBEROFCOPIESREQUIRED'TTR

19ENCL19

IndianaMichiganPowerCompanyP.O.Box16631Columbus,

OH43216INDIANANICHIGANPOWERAEP;NRC'1212G

10CFR2.201DonaldC.CookNuclearPlantUnits1and2DocketNos.50-315and50-316LicenseNos.DPR-58andDPR-74NRCINSPECTION

REPORTSNO.50-315/94013

(DRP)AND50-316/94013

(DRP)REPLYTONOTICEOFVIOLATION

U.S.NuclearRegulatory

Commission

DocumentControlDeskWashington,

D.C.20555Attn:Mr.J.B.MartinAugust19,1994DearMr.Martin:ThisletterisinresponsetoaUSNRCletterdatedJuly20,1994,thatforwarded

anoticeofviolation

toIndianaMichiganPowerCompany.Thenoticeofviolation

contained

oneviolation

identified

duringaroutinesafetyinspection

conducted

byMessrs.J.A.Isom,D.J.Hartland,

andD.L.ShepardfromJune4,1994,throughJuly1,1994.Theviolation

isassociated

withtherepeatedpackingfailuresofaUnit2mainsteamtestselectorvalveoveraperiodoftwoyearsthatresultedinseveralentriesintofour-hour

limitingconditions

ofoperation.

Ourreplytothenoticeofviolation

isprovidedintheattachment

tothisletter.Thisletterissubmitted

pursuantto10CFR50.54(f)and,assuch,anoathstatement

isattached.

p~W)VicePresident

arAttachment

940S240071

94081PDRADDCI;05000315PDFi'gy/

Mr.J.B.Martin-2-AEP:NRC:1212G

CC:A.A.BlindG.CharnoffW.T.Russell,NRC-Washington,

D.C.NRCResidentInspector

NFEMSectionChiefJ.R.Padgett

STATEOFOHIOCOUNTYOFFRANKLINE.E.Fitzpatrick,

beingdulysworn,deposesandsaysthatheistheVicePresident

oflicenseeIndianaMichiganPowerCompany,thathehasreadtheforegoing

responsetoNRCINSPECTION

REPORTSNO.50-315/94013

(DRP)AND50-316/94013

(DRP),REPLYTONOTICEOFVIOLATION

andknowsthecontentsthereof;andthatsaidcontentsaretruetothebestofhisknowledge

andbelief.Subscribed

endsworntobeforemethis~PEdayof19~EXNOTARYPUBLICAleD.HILLgpgpypUQUC,STAIEpFplllpSSXSSh',IEISSISS

EXPIRES~

ATTACHMENT

TOAEP:NRC:1212G

REPLYTONOTICEOFVIOLATION

ATTACHMENT

TOAEP:NRC:1212G

Page1Background

Aroutinesafetyinspection

wasconducted

byMessrs.JamesA.Isom,DavidJ.Hartland,

andDouglasL.ShepardfromJurie4,1994,throughJuly1,1994.Duringthisinspection,

oneitemwasfoundtobeinviolation.

Theviolation

wasidentified

asthefailuretocorrectcherootcausefortherepeatedpackingfailuresofaUnit2mainsteamtestselectorvalveoveraperiodoftwoyearsthatresultedinseveralentriesintofour-hour

limitingconditions

ofoperation.

Thisviolation

wassetforthinalettercontaining

thenoticeofviolation,

datedJuly20,1994,fromMr.E.G.Greenman,

Director,

DivisionofReactorProjects,

USNRC,RegionIII.TheletterwasreceivedJuly25,1994.Ourresponsetothenoticeofviolation

iscontained

withinthisdocument.

NRCViolation

"10CFR50,AppendixB,Criterion

XVI,"Corrective

Action,"requiresinpartthat"Measures

shallbeestablished

toassurethatconditions

adversetoqualityarepromptlyidentified

andcorrected.

Inthecaseofsignificant

conditions

adversetoquality,themeasuresshallassurethatthecauseofthecondition

isdetermined

andcorrective

actiontakentoprecluderepetition."

Contrarytotheabove,asofJuly1,1994,thelicenseefailedtoreplacethepittedvalvestemonmainsteamstopvalve(MSSV)dumpvalvetestselector,

2-MM0-240,

asignificant

condition

adversetoquality.Specifically,

ActionRequest25594hadbeenwrittenonJuly8,'992,toreplacethepittedvalvestembutwasnotscheduled

tobeperformed

untiltherefueling

outagestartinginSeptember

1994.Consequently,

2-MMO-240

hadtoberepackedfivetimes,requiring

entriesintothefourhourLimitingCondition

ofOperation

(LCO),asrequiredbyTechnical

Specification

(TS)4.7.1.5.1.

Therewereseveralopportunities

sinceJuly1992toreplacethestemwithoutenteringtheLCO.ThisisaSeverityLevelIVviolation

(Supplement

I).

ATTACHMENT

TOAEP:NRC:1212GPage2ResponsetoViolation

dmissioorDenialotheAlleedViolatoIndianaMichiganPowerCompanyadmitstotheviolation

ascitedintheNRCnoticeofviolation.

2.easonsfortheViolatioTherootcauseforthisviolation

hasbeenidentified

asaprogrammatic

weaknessintheplant'scorrective

actionprogram.InJuly1992,Unit2wasinMode3(HotStandby).

Whilerepacking

2-MM0-240,

thevalvestemwasfoundtobepitted,scoredandinneedofreplacement.

AtthattimeanActionRequestwasinitiated

toreplacethestem.SincearepairactivityofthistyperequirescooldowntoMode5toperform,ascheduling

codeofU2R94wasassigned,

addingtherepairtothescopeofthe1994refueling

outage.AtthetimetheU2R94codewasassigned,

intheabsenceofpriorfailurehistory,thiswasthecorrectdesignation.

Thevalvestemreplacement

wouldonlyhavebeenelevatedtotheforcedoutagescheduleifthesubsequent,

repeatedrepairshadbeenidentified

asreworkandanadversetrend.Sincethevalvestemdeficiency

wasfirstidentified,

2-MMO-240

hasbeenrepackedfiveadditional

times.Hadthevalvestemreplacement

beenscheduled

asaforcedoutageactivity,

therewouldhavebeentwoopportunities

priortotheviolation

tocompletetherepair.Thefirstopportunity

occurredinAugust1993whentheunitexperienced

areactortripandforcedoutage.Thesecondopportunity

occurredinJanuary1994whentheunitwasremovedfromservicetorepairanunisolable

steamleakonSteamGenerator

21blowdownline.Repeatedpackingreplacements

werenotidentified

intheplant'sCorrective

ActionProgram(PMI-7030)

asanadversetrend.PMI-7030,

"Corrective

ActionProgram,"

requiresacondition

reporttobewrittenforsimilarcorrective

maintenance

workwithin90daysoftheoriginaldeficiency.

OnlythefinalpackingfailureonMay17,1994,fellwithinthe90daycriteria,

asthisfailureoccurred57daysafterthepreviousrepaironMarch21,1994.

ATTACHMENT

TOAEP:NRC:12120Page3Areworkcondition

reportwasnotinitiated

following

theMay17failureduetoanerrorintheMaintenance

Administrative

Procedure

(MAP)¹MA3.3-05,

"Maintenance

Planning".

MAP¹MA3.3-05

incorrectly

definedreworkassimilarworkperformed

within30daysoftheoriginalfailure,ratherthan90days.Asaresultofthiserrorthemaintenance

plannerfailedtoidentifythereoccurrence

ofthepackingleakonMay17,1994,asfallingwithinthedefinition

ofrework.3.CorectiveActionsTakenandesultseyedTheworkcontrolprocesscodewaschangedonthe2-MMO-240

repairJobOrder.The2-MMO-240

repairtasknowappearsontheforcedoutageschedule,

aswellaswithinthescopeoftherefueling

outage.MAP¹MA3.3-05,

"Maintenance

Planning,"

wasrevisedtoreflectthecurrentdefinition

ofreworkcontained

inPMI-7030.4.Corrective

ActionsTakentoAvoidFurtherViolations

PMI-7030,

"Corrective

Action,"willberevisedtoredefinerework.Thedefinition

forreworkwillnowincludeanycorrective

maintenance

whichrequiresentryintoaLimitingCondition

ofOperation

(LCO)ifsimilarworkhasbeenperformed

onthatequipment/component

duringthecurrentoperating

cycle,including

thepreviousrefueling

outage.Whenreworkofthistypeoccurs,aCondition

Reportwillbewrittentoaidintheidentification/evaluation

ofanadversetrend.The"90-day"standardwillberetainedforworkuponequipment

orcomponents

whichdonotinitiateanLCOentry.MAP¹MA3.3-05,

"Maintenance

Planning,"

willberevisedtorefertoPMI-7030fortheabove-described

redefinition

ofrework.Thesemeasureswillassurethatthistypeofcondition

willbeprecluded

inthefuture.5.ateWhenFullComlieneeWillBeAchievedPMI-7030andMAPmodifications

willbecompleted

bySeptember

30,1994.

ATTACHMENT

TOAEP:NRC:1212G

Page4Thevalvestemreplacement

for2-MMO-240

willbecompleted

duringthefirstMode5forcedoutageofsufficient

durationortheupcomingUnit2refueling

outage,scheduled

tocommenceSeptember

6,1994,whichever

occursfirst.