ML17341B170: Difference between revisions

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{{#Wiki_filter:December 7, 2017
{{#Wiki_filter:December 7, 2017  
   
   
Mr. Fadi Diya, Senior Vice President   and Chief Nuclear Officer Ameren Missouri  
Mr. Fadi Diya, Senior Vice President
  and Chief Nuclear Officer Ameren Missouri  
Callaway Plant  
Callaway Plant  
P.O. Box 620  
P.O. Box 620  
Fulton, MO 65251  SUBJECT: CALLAWAY PLANT - RESPONSE TO NOTICE OF VIOLATION (NRC INSPECTION REPORT 05000483/2017007)   
Fulton, MO 65251  
Dear Mr. Diya:  On August 28, 2017, the U.S. Nuclear Regulatory Commission (NRC) cited Union Electric  
  SUBJECT: CALLAWAY PLANT - RESPONSE TO NOTICE OF VIOLATION (NRC INSPECTION REPORT 05000483/2017007)  
   
Dear Mr. Diya:  
  On August 28, 2017, the U.S. Nuclear Regulatory Commission (NRC) cited Union Electric  
Company for failure to restore compliance for a Technical Specification 5.4.1.a. violation  
Company for failure to restore compliance for a Technical Specification 5.4.1.a. violation  
associated with the failure to perform preventative maintenance procedures to verify the  
associated with the failure to perform preventative maintenance procedures to verify the  
operation and timing of the engineered safety feature transformer XNBOl load tap changer at the Callaway Plant.  The Notice of Violation (Notice), enclosed within NRC Inspection Report 05000458/2017007 (ML17283A392), required you to respond in writing within 30 days.   
operation and timing of the engineered safety feature transformer XNBOl load tap changer at the Callaway Plant.  The Notice of Violation (Notice), enclosed within NRC Inspection Report 05000458/2017007 (ML17283A392), required you to respond in writing within 30 days.  
   
You responded to the Notice by letter, dated November 1, 2017 (ML17306A103).  In your  
You responded to the Notice by letter, dated November 1, 2017 (ML17306A103).  In your  
response, you stated that the timing of engineered safety feature transformer XNBOl load tap changer was successfully tested on October 20, 2017, thus resolving the technical issue associated with the violation for not previously verifying the operation and timing of the load tap changer.  You also responded that timing testing of engineered safety feature  
response, you stated that the timing of engineered safety feature transformer XNBOl load tap changer was successfully tested on October 20, 2017, thus resolving the technical issue associated with the violation for not previously verifying the operation and timing of the load tap changer.  You also responded that timing testing of engineered safety feature  
transformers XNBOl and XNB02 load tap changers will continue to be performed on a routine  
transformers XNBOl and XNB02 load tap changers will continue to be performed on a routine  
basis, going forward.  The letter also indicated that you are reviewing any NRC violations received since October 2015 for jobs that you are crediting for restoring compliance.  The basis  
basis, going forward.  The letter also indicated that you are reviewing any NRC violations received since October 2015 for jobs that you are crediting for restoring compliance.  The basis  
for selecting October 2015 was that this was the last time a comprehensive pre-Problem Identification and Resolution (Pl&R) inspection self-assessment was performed.  In that assessment, the timeliness of corrective actions for NRC violations prior to October 2015 had been evaluated.   
for selecting October 2015 was that this was the last time a comprehensive pre-Problem Identification and Resolution (Pl&R) inspection self-assessment was performed.  In that assessment, the timeliness of corrective actions for NRC violations prior to October 2015 had  
been evaluated.   
 
   
   
We have reviewed your response letter and find that it meets the requirements of 10 CFR 2.201.  The adequacy of your corrective actions to the Notice will be reviewed and, if found acceptable, will be closed in the resident inspector integrated inspection report.  
We have reviewed your response letter and find that it meets the requirements of 10 CFR 2.201.  The adequacy of your corrective actions to the Notice will be reviewed and, if found acceptable, will be closed in the resident inspector integrated inspection report.  
   
   
    
    
F. Diya 2 This letter will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding."  Sincerely,  
F. Diya 2 This letter will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html
and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding.
"  Sincerely,  
 
  /RA/  Thomas R. Farnholtz, Chief Engineering Branch 1  
  /RA/  Thomas R. Farnholtz, Chief Engineering Branch 1  
Division of Reactor Safety   
 
Docket No. 50-483 License No. NPF-30   
Division of Reactor Safety  
   
Docket No. 50-483 License No. NPF-30  
   
Electronic Distribution for Callaway Plant   
Electronic Distribution for Callaway Plant   


   ML17341B170  SUNSI Review  ADAMS:    Non-Publicly Available  Non-Sensitive Keyword:  By:  RAK  Yes    No  Publicly Available  Sensitive  NRC-002 OFFICE SRI/EB1 C/EB1 C/PBB C:EB1  NAME RKopriva TFarnholtz NTaylor TFarnholtz  SIGNATURE /RA/  TRF for /RA/ /RA/ /RA/  DATE 12/7/17 12/7/17 12/7/1712/7/17
   ML17341B170  SUNSI Review  ADAMS:    Non-Publicly Available  Non-Sensitive Keyword:  By:  RAK  Yes    No  Publicly Available  Sensitive  NRC-002 OFFICE SRI/EB1 C/EB1 C/PBB C:EB1  NAME RKopriva TFarnholtz NTaylor TFarnholtz  SIGNATURE /RA/  TRF for /RA/ /RA/ /RA/  DATE 12/7/17 12/7/17 12/7/17
12/7/17
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Revision as of 05:56, 29 June 2018

Callaway Plant - Response to Notice of Violation (NRC Inspection Report 05000483/2017007)
ML17341B170
Person / Time
Site: Callaway Ameren icon.png
Issue date: 12/07/2017
From: Thomas Farnholtz
Division of Reactor Safety IV
To: Diya F
Ameren Missouri
References
IR 2017007
Download: ML17341B170 (3)


See also: IR 05000483/2017007

Text

December 7, 2017

Mr. Fadi Diya, Senior Vice President

and Chief Nuclear Officer Ameren Missouri

Callaway Plant

P.O. Box 620

Fulton, MO 65251

SUBJECT: CALLAWAY PLANT - RESPONSE TO NOTICE OF VIOLATION (NRC INSPECTION REPORT 05000483/2017007)

Dear Mr. Diya:

On August 28, 2017, the U.S. Nuclear Regulatory Commission (NRC) cited Union Electric

Company for failure to restore compliance for a Technical Specification 5.4.1.a. violation

associated with the failure to perform preventative maintenance procedures to verify the

operation and timing of the engineered safety feature transformer XNBOl load tap changer at the Callaway Plant. The Notice of Violation (Notice), enclosed within NRC Inspection Report 05000458/2017007 (ML17283A392), required you to respond in writing within 30 days.

You responded to the Notice by letter, dated November 1, 2017 (ML17306A103). In your

response, you stated that the timing of engineered safety feature transformer XNBOl load tap changer was successfully tested on October 20, 2017, thus resolving the technical issue associated with the violation for not previously verifying the operation and timing of the load tap changer. You also responded that timing testing of engineered safety feature

transformers XNBOl and XNB02 load tap changers will continue to be performed on a routine

basis, going forward. The letter also indicated that you are reviewing any NRC violations received since October 2015 for jobs that you are crediting for restoring compliance. The basis

for selecting October 2015 was that this was the last time a comprehensive pre-Problem Identification and Resolution (Pl&R) inspection self-assessment was performed. In that assessment, the timeliness of corrective actions for NRC violations prior to October 2015 had

been evaluated.

We have reviewed your response letter and find that it meets the requirements of 10 CFR 2.201. The adequacy of your corrective actions to the Notice will be reviewed and, if found acceptable, will be closed in the resident inspector integrated inspection report.

F. Diya 2 This letter will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html

and at the NRC Public Document Room in accordance with 10 CFR 2.390, "Public Inspections, Exemptions, Requests for Withholding.

" Sincerely,

/RA/ Thomas R. Farnholtz, Chief Engineering Branch 1

Division of Reactor Safety

Docket No. 50-483 License No. NPF-30

Electronic Distribution for Callaway Plant

ML17341B170 SUNSI Review ADAMS: Non-Publicly Available Non-Sensitive Keyword: By: RAK Yes No Publicly Available Sensitive NRC-002 OFFICE SRI/EB1 C/EB1 C/PBB C:EB1 NAME RKopriva TFarnholtz NTaylor TFarnholtz SIGNATURE /RA/ TRF for /RA/ /RA/ /RA/ DATE 12/7/17 12/7/17 12/7/17

12/7/17