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  .        A Kffog                                 UNITED STATES
A Kffog
                      Do
UNITED STATES
        /             "
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                                        NUCLEAR REGULATORY COMMISSION
/
                                                      REGION ll
D
      ['
NUCLEAR REGULATORY COMMISSION
              -
o
                        n
['
      g'                 j                     101 MARIETTA STREET, N.W.
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      *                 's                     ATLANTA, GEORGI A 30323
"
        '4
REGION ll
          9 + . . . . ,o
n
    Report Nos.: 50-321/86-08 and 50-366/86-08                 ,
g'
    Licensee: Georgia Power Company
j
                        P. O. Box 4545
101 MARIETTA STREET, N.W.
                        Atlanta, GA 30302
*
    Docket Nos.: 50-321 and 50-366                               License Nos.: DPR-5.7 and NPF-5 ',
's
,
ATLANTA, GEORGI A 30323
    Facility Name: Hatch 1 and 2                                               -
'49 + . . . . ,o
Report Nos.: 50-321/86-08 and 50-366/86-08
,
Licensee: Georgia Power Company
P. O. Box 4545
Atlanta, GA 30302
Docket Nos.: 50-321 and 50-366
License Nos.: DPR-5.7 and NPF-5 ',
Facility Name: Hatch 1 and 2
-
,
1
1
j   Inspection Conducted: February 24 - March 3, 1986                       '
j
Inspection Conducted: February 24 - March 3, 1986
'
Inspectors:
Ah bk11:
3/26 l86
,
,
G. Seinebli
Date Signed
,
,
    Inspectors:            Ah bk11:
8 ,/M * At
                        G. Seinebli
3hd84
                                                                                    3/26 l86
'
                                                                                    Date Signed
K. Poertner
'
j
                          8 ,/M * At                                               3hd84
Date Signed
                        K. Poertner           j                                     Date Signed
MU
    Approved by:                                           ef:24L                 MU
Approved by:
                        F. Jape, Section Chief         (/ /                       Date Signed
ef:24L
                        Engineering Branch
F. Jape, Section Chief
                        Division of Reactor Safety
(/ /
                                                    SUMMARY
Date Signed
    Scope:       This routine, unannounced inspection entailed 120 inspector-hours at the
Engineering Branch
    site, in a review of maintenance programs and practices.
Division of Reactor Safety
    Results: Two violations were identified - (1) Failure to implement maintenance
SUMMARY
    controls and document conditions adverse to quality - paragraph 5.a. (2) Failure
Scope:
    to implement existing plant procedures properly - paragraphs 5.b. and 5.c.
This routine, unannounced inspection entailed 120 inspector-hours at the
                                                                                                      I
site, in a review of maintenance programs and practices.
                                                                                                      l
Results:
      9604100229 860404
Two violations were identified - (1) Failure to implement maintenance
      PDR       ADOCK 05000321 pnn
controls and document conditions adverse to quality - paragraph 5.a.
      a
(2) Failure
to implement existing plant procedures properly - paragraphs 5.b. and 5.c.
I
9604100229 860404
PDR
ADOCK 05000321
a
pnn
'
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  .
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                                  REPORT DETAILS
.
  1. Persons Contacted
REPORT DETAILS
      Licensee Employees
1.
      S. Barr, Maintenarce Supervisor
Persons Contacted
    *S. Brunson, Reactor Systems Engineer
Licensee Employees
      0. Fraser, Quality Assurance Audit Supervisor
S. Barr, Maintenarce Supervisor
    *P. Fornel, Manager of Quality Assurance
*S. Brunson, Reactor Systems Engineer
      R. Gatliff, Shift Supervisor
0. Fraser, Quality Assurance Audit Supervisor
      R. Glisson, Maintenance Engineering Supervisor
*P. Fornel, Manager of Quality Assurance
    *C. Goodman, Regulatory Compliance Engineer
R. Gatliff, Shift Supervisor
      R. Houston, Quality Concerns Coordinator
R. Glisson, Maintenance Engineering Supervisor
      R. Keck, Engineer Supervisor
*C. Goodman, Regulatory Compliance Engineer
      T. King, Maintenance Foreman
R. Houston, Quality Concerns Coordinator
      D. McCusker, Superintendent of Quality Control
R. Keck, Engineer Supervisor
      T. Metzler, Maintenance Engineer
T. King, Maintenance Foreman
    *D. Morgan, Engineering Supervisor
D. McCusker, Superintendent of Quality Control
    *H. Nix, General Manager
T. Metzler, Maintenance Engineer
    *T. Powers, Manager of Engineering
*D. Morgan, Engineering Supervisor
    *T. Seitz, Manager of Maintenance
*H. Nix, General Manager
    *B. Thigpen, Quality Assurance Specialist
*T. Powers, Manager of Engineering
      Other licensee employees contacted included outage craftsmen, engineers,
*T. Seitz, Manager of Maintenance
      technicians, operators, mechanics, and office personnel.
*B. Thigpen, Quality Assurance Specialist
      NRC Resident Inspectors
Other licensee employees contacted included outage craftsmen, engineers,
    *P. Holmes-Ray, Senior Resident Inspector
technicians, operators, mechanics, and office personnel.
      G. Nejfelt, Resident Inspector
NRC Resident Inspectors
    * Attended exit interview
*P. Holmes-Ray, Senior Resident Inspector
  2. Exit Interview                                                             -
G. Nejfelt, Resident Inspector
      The inspection scope and findings were summarized on March 3,1986, with
* Attended exit interview
      those persons indicated in paragraph 1 above. The inspectors described the
2.
      areas inspected and discussed in detail the inspection findings.   The
Exit Interview
      following new items were identified during this inspection:
-
      Violation 321/86-08-01, Failure to implement maintenance controls and
The inspection scope and findings were summarized on March 3,1986, with
      document conditions adverse to quality - paragraph 5.a.
those persons indicated in paragraph 1 above. The inspectors described the
      Violation 321/86-08-02, Failure to properly implement existing plant
areas inspected and discussed in detail the inspection findings.
      procedures - paragraphs 5.b and 5.c.
The
      Unresolved Item 321/86-08-03, Determine actual maintenance performed on
following new items were identified during this inspection:
      valve E11-F004B in 1981 - paragraph 5.d.
Violation 321/86-08-01, Failure to implement maintenance controls and
document conditions adverse to quality - paragraph 5.a.
Violation 321/86-08-02, Failure to properly implement existing plant
procedures - paragraphs 5.b and 5.c.
Unresolved Item 321/86-08-03, Determine actual maintenance performed on
valve E11-F004B in 1981 - paragraph 5.d.


    _.                                                                           _
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                                              2
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2
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l        Proprietary material was reviewed during the course of this inspection,
i        however, the information is not contained in this report.
      3. Licensee Action on Previous Enforcement Matters
l
l
          This subject was not addressed in the inspection.
Proprietary material was reviewed during the course of this inspection,
      4. Unresolved Items
i
          An unresolved Item is a matter about which more information is required to
however, the information is not contained in this report.
i         determine whether it is acceptable or may involve a violation or deviation.
3.
t        One new unresolved item identified during this inspection is discussed in
Licensee Action on Previous Enforcement Matters
          paragraph 5.d.
l
      5. Review Of The Maintenance Program and Practices (62702)
This subject was not addressed in the inspection.
          This inspection was conducted to review the licensee's maintenance program
4.
          and maintenance practices in the area of valve repairs accomplished during
Unresolved Items
          the current Unit 1 outa       An in depth review of valve maintenance in the
An unresolved Item is a matter about which more information is required to
          Residual Heat Removal (ge.RHR) System was performed. In this inspection, the
i
          following documents were reviewed:
determine whether it is acceptable or may involve a violation or deviation.
          *
One new unresolved item identified during this inspection is discussed in
                50AC-MNT-001-05, Revision 4, Administrative Control Procedure       -
t
                Maintenance Program.
paragraph 5.d.
          *
5.
                32GM.MEL-022-05, Revision 0, General Maintenance Procedure - Limitorque
Review Of The Maintenance Program and Practices (62702)
                Valve Operator Electrical Maintenance.
This inspection was conducted to review the licensee's maintenance program
          *
and maintenance practices in the area of valve repairs accomplished during
                10AC-MGR04-0, Revision 0, Administrative Control Procedure - Deficiency
the current Unit 1 outa
                Control System.
An in depth review of valve maintenance in the
          *
Residual Heat Removal (ge.RHR) System was performed.In this inspection, the
                40AC-ENG03-0, Revision 0, Administrative Control Procedure - Design
following documents were reviewed:
                Control.
*
          *
50AC-MNT-001-05, Revision 4,
                52CM-MME-011-OS, Revision 0, Corrective Maintenance Procedure - Gate
Administrative Control Procedure
                and Globe Valve Repair.
-
                52-PM-MME-010-0, Revision 0, Preventive Maintenance Procedure - Safety
Maintenance Program.
                and Relief Valve Maintenance.
*
32GM.MEL-022-05, Revision 0, General Maintenance Procedure - Limitorque
Valve Operator Electrical Maintenance.
*
10AC-MGR04-0, Revision 0, Administrative Control Procedure - Deficiency
Control System.
*
40AC-ENG03-0, Revision 0, Administrative Control Procedure - Design
Control.
52CM-MME-011-OS, Revision 0, Corrective Maintenance Procedure - Gate
*
and Globe Valve Repair.
52-PM-MME-010-0, Revision 0, Preventive Maintenance Procedure - Safety
and Relief Valve Maintenance.
!
!
          *
!
!              50AC-MTL-002-05, Revision 1,   Administrative Control Procedure     -
*
                Identification and Control of Material and Equipment.
50AC-MTL-002-05, Revision 1,
                40AC-QCX-001-0, Revision 0, Administrative Control Procedure - Quality
Administrative Control Procedure
-
Identification and Control of Material and Equipment.
40AC-QCX-001-0, Revision 0, Administrative Control Procedure - Quality
.
.
                Control Inspection Program
Control Inspection Program
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!         *
!
                42EN-ENG-009-0, Revision 2, Engineering Procedure - Equivalent Deter-
*
l              mination of Replacement Parts or Materials.
42EN-ENG-009-0, Revision 2, Engineering Procedure - Equivalent Deter-
          *
                Maintenance Work order (MW0),1-85-7214 - Work Performed on Valve
                1E11-F0158.
l
l
mination of Replacement Parts or Materials.
Maintenance Work order (MW0),1-85-7214 - Work Performed on Valve
*
1E11-F0158.
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                                                                                      1
.
      .
.
    .
3
                                              3
MW0, 1-85-7330 - Work Performed on Valve 1E11-F0178.
              MW0, 1-85-7330 - Work Performed on Valve 1E11-F0178.
MWO, 1-85-7120 - Work Performed on Valve 1E11-F004A.
  ..          MWO, 1-85-7120 - Work Performed on Valve 1E11-F004A.
..
              MWO, 1-85-7216 - Work Performed on Valve 1E11-F0308.
MWO, 1-85-7216 - Work Performed on Valve 1E11-F0308.
        '
MWO, 1-85-7019 - Work Performed on Valve 1E11-F007A.
              MWO, 1-85-7019 - Work Performed on Valve 1E11-F007A.
'
              MW0, 1-85-7118 - Work Performed on Valve 1E11-F028A.
MW0, 1-85-7118 - Work Performed on Valve 1E11-F028A.
              MWO, 1-85-7672 - Work Performed on Valve 1E11-F025A.
MWO, 1-85-7672 - Work Performed on Valve 1E11-F025A.
              MW0, 1-85-7119 - Work Performed en Valve IE11-F0078.
MW0, 1-85-7119 - Work Performed en Valve IE11-F0078.
              MW0, 1-86-0615 - Work Performed on Valve IE11-F0248.
MW0, 1-86-0615 - Work Performed on Valve IE11-F0248.
              MWO, 1-85-7215 - Work Performed on Valve 1E11-F0288.
MWO, 1-85-7215 - Work Performed on Valve 1E11-F0288.
              MWO, 1-85-7217 - Work Performed on Valve IE11-TRV.
MWO, 1-85-7217 - Work Performed on Valve IE11-TRV.
              MWO, 1-81-3328 - Work Performed on Valve IE11-0048.
MWO, 1-81-3328 - Work Performed on Valve IE11-0048.
              MW0, 1-86-0472 - Additional Work Performed on Valves 1E11-F028A and
MW0, 1-86-0472 - Additional Work Performed on Valves 1E11-F028A and
              1E11-F0288.
1E11-F0288.
        "
"
              MW0, 1-86-0987 - Additional Work Performed on Valves 1E11-F024A.
MW0, 1-86-0987 - Additional Work Performed on Valves 1E11-F024A.
              MWO, 1-86-1155 - Additional Work Performed on Valves 1E11-F004A.
MWO, 1-86-1155 - Additional Work Performed on Valves 1E11-F004A.
        In the review of the documents listed above, the following deficiencies were
In the review of the documents listed above, the following deficiencies were
        noted:
noted:
        a.   Maintenance Work Order (MWO) 1-85-7120 was initiated to repair valve
a.
              1E11-F004A, RHR torus suction valve.       During inspection of the
Maintenance Work Order (MWO) 1-85-7120 was initiated to repair valve
              internals of the valve, it was determined that the valve wedge had to
1E11-F004A, RHR torus suction valve.
              be replaced and a replacement wedge was obtained from supply using
During inspection of the
              Purchase Order 7666. During assembly of the valve wedge to the valve
internals of the valve, it was determined that the valve wedge had to
              stem, it was determined that the replacement wedge did not fit the
be replaced and a replacement wedge was obtained from supply using
              original stem supplied with the E11-F004A valve. The valve stem had a
Purchase Order 7666.
              "T" head configuration whereas the wedge slot had an hourglass
During assembly of the valve wedge to the valve
              configuration. The maintenance supervisor, a Crane Valve employee,
stem, it was determined that the replacement wedge did not fit the
              directed his maintenance personnel to grind down the valve stem to make
original stem supplied with the E11-F004A valve.
              the replacement wedge fi t . The grindin'g of the valve stem was
The valve stem had a
              accomplished on the verbal instructions of the maintenance supervisor
"T" head configuration whereas the wedge slot had an hourglass
              and was not documented in the work package reviewed by the inspectors.
configuration.
              Upon discovery by the licensee, efforts were made to obtain a replace-
The maintenance supervisor, a Crane Valve employee,
              ment stem with the hourglass design. The licensee was unable to obtain
directed his maintenance personnel to grind down the valve stem to make
              a replacement stem with the hourglass design due to outage limitations
the replacement wedge fi t .
              and delivery constraints, so Crane Valve Services contacted ALOYC0 who
The grindin'g of the valve stem was
accomplished on the verbal instructions of the maintenance supervisor
and was not documented in the work package reviewed by the inspectors.
Upon discovery by the licensee, efforts were made to obtain a replace-
ment stem with the hourglass design.
The licensee was unable to obtain
a replacement stem with the hourglass design due to outage limitations
and delivery constraints, so Crane Valve Services contacted ALOYC0 who
i
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.
. .
. . .
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  .
.
                                      4
4
      contacted Walworth, the valve manufacturer, with a proposal for a
contacted Walworth, the valve manufacturer, with a proposal for a
!      temporary fix to utilize the existing stem until the next available
      outage when a proper stem replacement could be made. Walworth provided
      a sketch to modify the "T" head stem arrangement to approximate the
      hourglass stem arrangement that per the Hatch drawings should have been
      installed in the valve. No attempt was made to determine why a "T"
      head stem and wedge were originally installed in the valve, nor was a
      design change request initiated to modify the existing stem.
l      10 CFR 50 Appendix B Criterion XVI states:    Measures shall be estab-
!
!
      lished to assure that conditions adverse to quality such as failures,
temporary fix to utilize the existing stem until the next available
j     malfunctions, deficiencies, deviations, defective material and equip-
outage when a proper stem replacement could be made. Walworth provided
      ment and nonconformance are promptly identified and corrected.
a sketch to modify the "T" head stem arrangement to approximate the
hourglass stem arrangement that per the Hatch drawings should have been
installed in the valve.
No attempt was made to determine why a "T"
head stem and wedge were originally installed in the valve, nor was a
design change request initiated to modify the existing stem.
l
10 CFR 50 Appendix B Criterion XVI states:
Measures shall be estab-
lished to assure that conditions adverse to quality such as failures,
!
j
malfunctions, deficiencies, deviations, defective material and equip-
ment and nonconformance are promptly identified and corrected.
10 CFR 50 Appendix B Criterion V states: Activities affectinJ quality
,
,
      10 CFR 50 Appendix B Criterion V states: Activities affectinJ quality
shall be prescribed by documented instructions, procedures or drawings,
      shall be prescribed by documented instructions, procedures or drawings,
of a type appropriate to the circumstances and shall be accomplished in
      of a type appropriate to the circumstances and shall be accomplished in
accordance with these instructions, procedures, or drawings.
      accordance with these instructions, procedures, or drawings. Instruc-
Instruc-
      tions, procedures, or drawings shall include appropriate quantitative
tions, procedures, or drawings shall include appropriate quantitative
      or qualitative acceptance criteria for determining that important
or qualitative acceptance criteria for determining that important
      activities have been satisfactorily accomplished.
activities have been satisfactorily accomplished.
      Hatch procedure 10AC-MGR04-0, Deficiency Control System, step 8.2
Hatch procedure 10AC-MGR04-0, Deficiency Control System, step 8.2
      states significant conditions adverse to quality will normally require
states significant conditions adverse to quality will normally require
      initiation of a Deficiency Report (DR). During the operations Phase of
initiation of a Deficiency Report (DR). During the operations Phase of
      plant Hatch, the conditions described in Attachment 1 shall be
plant Hatch, the conditions described in Attachment 1 shall be
      considered Significant Conditions adverse to Quality.
considered Significant Conditions adverse to Quality.
1
1
'
'
      Attachment 1 of 10AC-MGR04-0 states that negligence or disregard of
Attachment 1 of 10AC-MGR04-0 states that negligence or disregard of
      management policy defined in administrative controls or procedural
management policy defined in administrative controls or procedural
      requirements is a significant condition adverse to quality.
requirements is a significant condition adverse to quality.
      Contrary to the above, when it was determined that the replacement
Contrary to the above, when it was determined that the replacement
wedge for valve IE11-F004A did not fit the original stem, the stem was
,
,
      wedge for valve IE11-F004A did not fit the original stem, the stem was
ground down to make the replacement wedge fit.
This modification of
'
'
      ground down to make the replacement wedge fit. This modification of
the original stem was accomplished on the verbal authorization of the
      the original stem was accomplished on the verbal authorization of the
maintenance supervisor only.
      maintenance supervisor only. No deficiency report was initiated to
No deficiency report was initiated to
      document that the replacement wedge did not correspond tn the as-found
document that the replacement wedge did not correspond tn the as-found
      condition of the valve or that modification of the original stem had
condition of the valve or that modification of the original stem had
l     been accomplished by disregarding the administrative controls and       ,
l
j     procedural requirements of the Hatch Maintenance program. This is       )
been accomplished by disregarding the administrative controls and
      identified as a Violation 50-321/86-08-01, Failure to implement main-
,
      tenance controls and document conditions adverse to quality.     Review
j
      of this violation is continuing, therefore, it is not included in the
procedural requirements of the Hatch Maintenance program.
      Notice of Violation.
This is
                                                                              1
)
    b. Maintenance Work Order 1-85-7217 worked the IE11-thermal relief valve
identified as a Violation 50-321/86-08-01, Failure to implement main-
      on the RHR side of the "B" RHR heat exchanger. The inspectors reviewed 1
tenance controls and document conditions adverse to quality.
      the work package associated with this work and noted no discrepancies
Review
      in the paper work provided for review. Per the work package, the valve
of this violation is continuing, therefore, it is not included in the
      had been removed, repaired, reinstalled and tested in accordance with
Notice of Violation.
1
b.
Maintenance Work Order 1-85-7217 worked the IE11-thermal relief valve
on the RHR side of the "B" RHR heat exchanger. The inspectors reviewed
1
the work package associated with this work and noted no discrepancies
in the paper work provided for review.
Per the work package, the valve
had been removed, repaired, reinstalled and tested in accordance with
i
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                                        5
.
l       approved procedures.   Review of the RHR Piping and Instrument Diagram
5
l       determined that there are two thermal relief valves associated with the
l
        RHR heat exchanger. One relief valve is located on the RHR side of the
approved procedures.
        heat exchanger and one relief valve is located on the RHR service water
Review of the RHR Piping and Instrument Diagram
        side of the heat exchanger.     The inspectors inspected both relief
l
        valves. The RHR side relief valve did not appear to have been worked.
determined that there are two thermal relief valves associated with the
        The RHR service water side relief valve appeared refurbished and had a
RHR heat exchanger. One relief valve is located on the RHR side of the
l       valve leak repair yellow tag that referenced MWO 1-85-7217. When
heat exchanger and one relief valve is located on the RHR service water
        informed by the inspectors that the wrong thermal relief valve had been
side of the heat exchanger.
        repaired by MWO 1-85-7217 the licensee verified that the thermal relief
The inspectors inspected both relief
        valve on the RHR service water side of the "B" RHR Heat Exchanger had
valves.
        been worked instead of the thermal relief valve located or. the RHR side
The RHR side relief valve did not appear to have been worked.
        of the heat exchanger as required by MWO 1-85-7217.
The RHR service water side relief valve appeared refurbished and had a
        Failure to properly implement the maintenance program as defined in
l
!       Administrative Procedure 50AC-MNT-001-005, Maintenance Program is
valve leak repair yellow tag that referenced MWO 1-85-7217.
When
informed by the inspectors that the wrong thermal relief valve had been
repaired by MWO 1-85-7217 the licensee verified that the thermal relief
valve on the RHR service water side of the "B" RHR Heat Exchanger had
been worked instead of the thermal relief valve located or. the RHR side
of the heat exchanger as required by MWO 1-85-7217.
Failure to properly implement the maintenance program as defined in
!
Administrative Procedure 50AC-MNT-001-005, Maintenance Program is
identified as a Violation 50-321/86-08-02, Failure to properly imple-
'
'
        identified as a Violation 50-321/86-08-02, Failure to properly imple-
ment existing plant procedures.
        ment existing plant procedures.
c.
      c. Maintenance Work Order (MWO) 1-84-5742 worked the limitorque operator
Maintenance Work Order (MWO) 1-84-5742 worked the limitorque operator
        on valve IE11-F1038, one of the RHR Heat exchanger vent valves. This
on valve IE11-F1038, one of the RHR Heat exchanger vent valves. This
        MWO required the perfomance of procedure 52GM-MEL-022-05, Limitorque
MWO required the perfomance of procedure 52GM-MEL-022-05, Limitorque
        Valve Operator Electrical Maintenance. Section 7.9 of procedure
Valve Operator Electrical Maintenance.
        52GM-MEL-022-05 performs the preoperational set up and test of the
Section 7.9 of procedure
        limitorque valve operator.     Review of the completed work package
52GM-MEL-022-05 performs the preoperational set up and test of the
        revealed that steps 7.9.13.7 through 7.9.13.17.1 were not performed
limitorque valve operator.
        during the performance of procedure 52GM-MEL-022-05. Section 7.9.13
Review of the completed work package
        performs the Electrical Circuit test of the limitorque operator prior
revealed that steps 7.9.13.7 through 7.9.13.17.1 were not performed
        to the operational test conducted in Section 10 of procedure
during the performance of procedure 52GM-MEL-022-05.
        52GM-MEL-022-05.
Section 7.9.13
        Procedure 52GM-MEL-022-0S did not allow for the omission of steps
performs the Electrical Circuit test of the limitorque operator prior
        7.9.13.7 through 7.9.13.17.1.
to the operational test conducted in Section 10 of procedure
        Technical Specification 6.8.1 requires that written procedures be
52GM-MEL-022-05.
        established, implemented, and maintained covering maintenance and
Procedure 52GM-MEL-022-0S did not allow for the omission of steps
        surveillance activities. Failure to properly implement maintenance
7.9.13.7 through 7.9.13.17.1.
        procedure 52GM-MEL-022-OS is identified as another example of Violation
Technical Specification 6.8.1 requires that written procedures be
        50-321/86-08-02.
established, implemented, and maintained covering maintenance and
      d. Inspector Review of Maintenance History records showed that valve
surveillance activities.
        1E11-F004B had its wedge replaced in 1981 by Maintenance Work Order
Failure to properly implement maintenance
        1-81-3328. Review of the work performed revealed that a replacement
procedure 52GM-MEL-022-OS is identified as another example of Violation
        wedge was obtained from the same purchase order used in the replacement
50-321/86-08-02.
d.
Inspector Review of Maintenance History records showed that valve
1E11-F004B had its wedge replaced in 1981 by Maintenance Work Order
1-81-3328.
Review of the work performed revealed that a replacement
wedge was obtained from the same purchase order used in the replacement
l
l
        of the wedge for the IE11-F004A valve. The inspectors expressed
of the wedge for the IE11-F004A valve.
        concern that the same "T" head type stem may have been originally
The inspectors expressed
        installed in IE11-F0048. The MWO package did not identify a problem
concern that the same "T" head type stem may have been originally
        between the stem and wedge fitup.       This item is identified as
installed in IE11-F0048.
        Unresolved Item 50-321/86-08-03 Determine actual maintenance performed
The MWO package did not identify a problem
        on valve E11-F004B in 1981, and must be resolved prior to Unit 1
between the stem and wedge fitup.
        startup.
This item is identified as
Unresolved Item 50-321/86-08-03 Determine actual maintenance performed
on valve E11-F004B in 1981, and must be resolved prior to Unit 1
startup.


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_
    .                                   .
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                                            6
o
l           Within the areas examined, two violations and one unrenlved item were
6
            identified.
l
    6. Management Meeting
Within the areas examined, two violations and one unrenlved item were
      On March 13, 1986, a management meeting was held between GPC,and the NRC in
identified.
6.
Management Meeting
On March 13, 1986, a management meeting was held between GPC,and the NRC in
the Region II Office.
The meeting was attended by senior GPC management,
.
.
      the Region II Office.      The meeting was attended by senior GPC management,
Crane Company Management, and Region II Management and staff.
      Crane Company Management, and Region II Management and staff. The purpose
The purpose
'
'
      of the meeting was to discuss the apparent lack of control in the valve
of the meeting was to discuss the apparent lack of control in the valve
      maintenance program, at Plant Hatch, based on the findings previously
maintenance program, at Plant Hatch, based on the findings previously
l
l
      addr.cssed in this inspection report.
addr.cssed in this inspection report.
      J. T. Beckham, Vice President and General Manager for Nuclear Generation,
J. T. Beckham, Vice President and General Manager for Nuclear Generation,
      opened the meeting for GPC by discussing their policies in regard to
opened the meeting for GPC by discussing their policies in regard to
      Regulatory Requirements and Quality Assurance. Additional discussions were
Regulatory Requirements and Quality Assurance. Additional discussions were
      introduced concerning GPC effort to increase the maintenance staff in order
introduced concerning GPC effort to increase the maintenance staff in order
      to reduce the number of contract personnel currently required for mainte-
to reduce the number of contract personnel currently required for mainte-
      nance.   In addition, Mr. Beckham, addressed the ongoing procedure upgrade
nance.
      program.   T. A. Seitz, Manager of Maintenance for Plant Hatch, lead the
In addition, Mr. Beckham, addressed the ongoing procedure upgrade
      discussion concerning GPC management systems which ensure quality work
program.
      and addressed the specific items of concern identified during this in-
T. A. Seitz, Manager of Maintenance for Plant Hatch, lead the
I     spection.     Mr. Beckham then closed the meeting with a summary and
discussion concerning GPC management systems which ensure quality work
I     indicated they would look further into the concerns identified in
and addressed the specific items of concern identified during this in-
      the maintenance program.
I
spection.
Mr. Beckham then closed the meeting with a summary and
I
indicated they would look further into the concerns identified in
the maintenance program.
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Latest revision as of 02:49, 24 May 2025

Insp Repts 50-321/86-08 & 50-366/86-08 on 860224-0303. Violations Noted:Failure to Implement Maint Controls, Document Conditions Adverse to Quality & Implement Existing Plant Procedures Properly
ML20199K791
Person / Time
Site: Hatch  Southern Nuclear icon.png
Issue date: 03/26/1986
From: Poertner K, Schnebli G
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20199K763 List:
References
50-321-86-08, 50-321-86-8, 50-366-86-08, 50-366-86-8, NUDOCS 8604100229
Download: ML20199K791 (7)


See also: IR 05000321/1986008

Text

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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REGION ll

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j

101 MARIETTA STREET, N.W.

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ATLANTA, GEORGI A 30323

'49 + . . . . ,o

Report Nos.: 50-321/86-08 and 50-366/86-08

,

Licensee: Georgia Power Company

P. O. Box 4545

Atlanta, GA 30302

Docket Nos.: 50-321 and 50-366

License Nos.: DPR-5.7 and NPF-5 ',

Facility Name: Hatch 1 and 2

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Inspection Conducted: February 24 - March 3, 1986

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Inspectors:

Ah bk11:

3/26 l86

,

G. Seinebli

Date Signed

,

8 ,/M * At

3hd84

'

K. Poertner

j

Date Signed

MU

Approved by:

ef:24L

F. Jape, Section Chief

(/ /

Date Signed

Engineering Branch

Division of Reactor Safety

SUMMARY

Scope:

This routine, unannounced inspection entailed 120 inspector-hours at the

site, in a review of maintenance programs and practices.

Results:

Two violations were identified - (1) Failure to implement maintenance

controls and document conditions adverse to quality - paragraph 5.a.

(2) Failure

to implement existing plant procedures properly - paragraphs 5.b. and 5.c.

I

9604100229 860404

PDR

ADOCK 05000321

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pnn

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REPORT DETAILS

1.

Persons Contacted

Licensee Employees

S. Barr, Maintenarce Supervisor

  • S. Brunson, Reactor Systems Engineer

0. Fraser, Quality Assurance Audit Supervisor

  • P. Fornel, Manager of Quality Assurance

R. Gatliff, Shift Supervisor

R. Glisson, Maintenance Engineering Supervisor

  • C. Goodman, Regulatory Compliance Engineer

R. Houston, Quality Concerns Coordinator

R. Keck, Engineer Supervisor

T. King, Maintenance Foreman

D. McCusker, Superintendent of Quality Control

T. Metzler, Maintenance Engineer

  • D. Morgan, Engineering Supervisor
  • H. Nix, General Manager
  • T. Powers, Manager of Engineering
  • T. Seitz, Manager of Maintenance
  • B. Thigpen, Quality Assurance Specialist

Other licensee employees contacted included outage craftsmen, engineers,

technicians, operators, mechanics, and office personnel.

NRC Resident Inspectors

  • P. Holmes-Ray, Senior Resident Inspector

G. Nejfelt, Resident Inspector

  • Attended exit interview

2.

Exit Interview

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The inspection scope and findings were summarized on March 3,1986, with

those persons indicated in paragraph 1 above. The inspectors described the

areas inspected and discussed in detail the inspection findings.

The

following new items were identified during this inspection:

Violation 321/86-08-01, Failure to implement maintenance controls and

document conditions adverse to quality - paragraph 5.a.

Violation 321/86-08-02, Failure to properly implement existing plant

procedures - paragraphs 5.b and 5.c.

Unresolved Item 321/86-08-03, Determine actual maintenance performed on

valve E11-F004B in 1981 - paragraph 5.d.

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Proprietary material was reviewed during the course of this inspection,

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however, the information is not contained in this report.

3.

Licensee Action on Previous Enforcement Matters

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This subject was not addressed in the inspection.

4.

Unresolved Items

An unresolved Item is a matter about which more information is required to

i

determine whether it is acceptable or may involve a violation or deviation.

One new unresolved item identified during this inspection is discussed in

t

paragraph 5.d.

5.

Review Of The Maintenance Program and Practices (62702)

This inspection was conducted to review the licensee's maintenance program

and maintenance practices in the area of valve repairs accomplished during

the current Unit 1 outa

An in depth review of valve maintenance in the

Residual Heat Removal (ge.RHR) System was performed.In this inspection, the

following documents were reviewed:

50AC-MNT-001-05, Revision 4,

Administrative Control Procedure

-

Maintenance Program.

32GM.MEL-022-05, Revision 0, General Maintenance Procedure - Limitorque

Valve Operator Electrical Maintenance.

10AC-MGR04-0, Revision 0, Administrative Control Procedure - Deficiency

Control System.

40AC-ENG03-0, Revision 0, Administrative Control Procedure - Design

Control.

52CM-MME-011-OS, Revision 0, Corrective Maintenance Procedure - Gate

and Globe Valve Repair.

52-PM-MME-010-0, Revision 0, Preventive Maintenance Procedure - Safety

and Relief Valve Maintenance.

!

!

50AC-MTL-002-05, Revision 1,

Administrative Control Procedure

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Identification and Control of Material and Equipment.

40AC-QCX-001-0, Revision 0, Administrative Control Procedure - Quality

.

Control Inspection Program

l

!

42EN-ENG-009-0, Revision 2, Engineering Procedure - Equivalent Deter-

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mination of Replacement Parts or Materials.

Maintenance Work order (MW0),1-85-7214 - Work Performed on Valve

1E11-F0158.

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MW0, 1-85-7330 - Work Performed on Valve 1E11-F0178.

MWO, 1-85-7120 - Work Performed on Valve 1E11-F004A.

..

MWO, 1-85-7216 - Work Performed on Valve 1E11-F0308.

MWO, 1-85-7019 - Work Performed on Valve 1E11-F007A.

'

MW0, 1-85-7118 - Work Performed on Valve 1E11-F028A.

MWO, 1-85-7672 - Work Performed on Valve 1E11-F025A.

MW0, 1-85-7119 - Work Performed en Valve IE11-F0078.

MW0, 1-86-0615 - Work Performed on Valve IE11-F0248.

MWO, 1-85-7215 - Work Performed on Valve 1E11-F0288.

MWO, 1-85-7217 - Work Performed on Valve IE11-TRV.

MWO, 1-81-3328 - Work Performed on Valve IE11-0048.

MW0, 1-86-0472 - Additional Work Performed on Valves 1E11-F028A and

1E11-F0288.

"

MW0, 1-86-0987 - Additional Work Performed on Valves 1E11-F024A.

MWO, 1-86-1155 - Additional Work Performed on Valves 1E11-F004A.

In the review of the documents listed above, the following deficiencies were

noted:

a.

Maintenance Work Order (MWO) 1-85-7120 was initiated to repair valve

1E11-F004A, RHR torus suction valve.

During inspection of the

internals of the valve, it was determined that the valve wedge had to

be replaced and a replacement wedge was obtained from supply using

Purchase Order 7666.

During assembly of the valve wedge to the valve

stem, it was determined that the replacement wedge did not fit the

original stem supplied with the E11-F004A valve.

The valve stem had a

"T" head configuration whereas the wedge slot had an hourglass

configuration.

The maintenance supervisor, a Crane Valve employee,

directed his maintenance personnel to grind down the valve stem to make

the replacement wedge fi t .

The grindin'g of the valve stem was

accomplished on the verbal instructions of the maintenance supervisor

and was not documented in the work package reviewed by the inspectors.

Upon discovery by the licensee, efforts were made to obtain a replace-

ment stem with the hourglass design.

The licensee was unable to obtain

a replacement stem with the hourglass design due to outage limitations

and delivery constraints, so Crane Valve Services contacted ALOYC0 who

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. .

. . .

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.

.

4

contacted Walworth, the valve manufacturer, with a proposal for a

!

temporary fix to utilize the existing stem until the next available

outage when a proper stem replacement could be made. Walworth provided

a sketch to modify the "T" head stem arrangement to approximate the

hourglass stem arrangement that per the Hatch drawings should have been

installed in the valve.

No attempt was made to determine why a "T"

head stem and wedge were originally installed in the valve, nor was a

design change request initiated to modify the existing stem.

l

10 CFR 50 Appendix B Criterion XVI states:

Measures shall be estab-

lished to assure that conditions adverse to quality such as failures,

!

j

malfunctions, deficiencies, deviations, defective material and equip-

ment and nonconformance are promptly identified and corrected.

10 CFR 50 Appendix B Criterion V states: Activities affectinJ quality

,

shall be prescribed by documented instructions, procedures or drawings,

of a type appropriate to the circumstances and shall be accomplished in

accordance with these instructions, procedures, or drawings.

Instruc-

tions, procedures, or drawings shall include appropriate quantitative

or qualitative acceptance criteria for determining that important

activities have been satisfactorily accomplished.

Hatch procedure 10AC-MGR04-0, Deficiency Control System, step 8.2

states significant conditions adverse to quality will normally require

initiation of a Deficiency Report (DR). During the operations Phase of

plant Hatch, the conditions described in Attachment 1 shall be

considered Significant Conditions adverse to Quality.

1

'

Attachment 1 of 10AC-MGR04-0 states that negligence or disregard of

management policy defined in administrative controls or procedural

requirements is a significant condition adverse to quality.

Contrary to the above, when it was determined that the replacement

wedge for valve IE11-F004A did not fit the original stem, the stem was

,

ground down to make the replacement wedge fit.

This modification of

'

the original stem was accomplished on the verbal authorization of the

maintenance supervisor only.

No deficiency report was initiated to

document that the replacement wedge did not correspond tn the as-found

condition of the valve or that modification of the original stem had

l

been accomplished by disregarding the administrative controls and

,

j

procedural requirements of the Hatch Maintenance program.

This is

)

identified as a Violation 50-321/86-08-01, Failure to implement main-

tenance controls and document conditions adverse to quality.

Review

of this violation is continuing, therefore, it is not included in the

Notice of Violation.

1

b.

Maintenance Work Order 1-85-7217 worked the IE11-thermal relief valve

on the RHR side of the "B" RHR heat exchanger. The inspectors reviewed

1

the work package associated with this work and noted no discrepancies

in the paper work provided for review.

Per the work package, the valve

had been removed, repaired, reinstalled and tested in accordance with

i

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_

,

i

.

5

l

approved procedures.

Review of the RHR Piping and Instrument Diagram

l

determined that there are two thermal relief valves associated with the

RHR heat exchanger. One relief valve is located on the RHR side of the

heat exchanger and one relief valve is located on the RHR service water

side of the heat exchanger.

The inspectors inspected both relief

valves.

The RHR side relief valve did not appear to have been worked.

The RHR service water side relief valve appeared refurbished and had a

l

valve leak repair yellow tag that referenced MWO 1-85-7217.

When

informed by the inspectors that the wrong thermal relief valve had been

repaired by MWO 1-85-7217 the licensee verified that the thermal relief

valve on the RHR service water side of the "B" RHR Heat Exchanger had

been worked instead of the thermal relief valve located or. the RHR side

of the heat exchanger as required by MWO 1-85-7217.

Failure to properly implement the maintenance program as defined in

!

Administrative Procedure 50AC-MNT-001-005, Maintenance Program is

identified as a Violation 50-321/86-08-02, Failure to properly imple-

'

ment existing plant procedures.

c.

Maintenance Work Order (MWO) 1-84-5742 worked the limitorque operator

on valve IE11-F1038, one of the RHR Heat exchanger vent valves. This

MWO required the perfomance of procedure 52GM-MEL-022-05, Limitorque

Valve Operator Electrical Maintenance.

Section 7.9 of procedure

52GM-MEL-022-05 performs the preoperational set up and test of the

limitorque valve operator.

Review of the completed work package

revealed that steps 7.9.13.7 through 7.9.13.17.1 were not performed

during the performance of procedure 52GM-MEL-022-05.

Section 7.9.13

performs the Electrical Circuit test of the limitorque operator prior

to the operational test conducted in Section 10 of procedure

52GM-MEL-022-05.

Procedure 52GM-MEL-022-0S did not allow for the omission of steps

7.9.13.7 through 7.9.13.17.1.

Technical Specification 6.8.1 requires that written procedures be

established, implemented, and maintained covering maintenance and

surveillance activities.

Failure to properly implement maintenance

procedure 52GM-MEL-022-OS is identified as another example of Violation

50-321/86-08-02.

d.

Inspector Review of Maintenance History records showed that valve

1E11-F004B had its wedge replaced in 1981 by Maintenance Work Order

1-81-3328.

Review of the work performed revealed that a replacement

wedge was obtained from the same purchase order used in the replacement

l

of the wedge for the IE11-F004A valve.

The inspectors expressed

concern that the same "T" head type stem may have been originally

installed in IE11-F0048.

The MWO package did not identify a problem

between the stem and wedge fitup.

This item is identified as

Unresolved Item 50-321/86-08-03 Determine actual maintenance performed

on valve E11-F004B in 1981, and must be resolved prior to Unit 1

startup.

_

.

.

o

6

l

Within the areas examined, two violations and one unrenlved item were

identified.

6.

Management Meeting

On March 13, 1986, a management meeting was held between GPC,and the NRC in

the Region II Office.

The meeting was attended by senior GPC management,

.

Crane Company Management, and Region II Management and staff.

The purpose

'

of the meeting was to discuss the apparent lack of control in the valve

maintenance program, at Plant Hatch, based on the findings previously

l

addr.cssed in this inspection report.

J. T. Beckham, Vice President and General Manager for Nuclear Generation,

opened the meeting for GPC by discussing their policies in regard to

Regulatory Requirements and Quality Assurance. Additional discussions were

introduced concerning GPC effort to increase the maintenance staff in order

to reduce the number of contract personnel currently required for mainte-

nance.

In addition, Mr. Beckham, addressed the ongoing procedure upgrade

program.

T. A. Seitz, Manager of Maintenance for Plant Hatch, lead the

discussion concerning GPC management systems which ensure quality work

and addressed the specific items of concern identified during this in-

I

spection.

Mr. Beckham then closed the meeting with a summary and

I

indicated they would look further into the concerns identified in

the maintenance program.

l

.

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