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# | {{Adams | ||
| number = ML042940585 | |||
| issue date = 10/07/2004 | |||
| title = September 2004 Monthly Operating Report for Beaver Valley Units 1 and 2 | |||
| author name = Pearce L | |||
| author affiliation = FirstEnergy Nuclear Operating Co | |||
| addressee name = | |||
| addressee affiliation = NRC/Document Control Desk, NRC/NRR | |||
| docket = 05000334, 05000412 | |||
| license number = DPR-066, NPF-073 | |||
| contact person = | |||
| case reference number = GL-97-002, L-04-133 | |||
| document type = License-Monthly Operating Report | |||
| page count = 3 | |||
}} | |||
=Text= | |||
{{#Wiki_filter:FENOC | |||
&~rsrrayt Nclear Oper~q ap9y_ | |||
Beaver Valley Power Station P. 0. Box 4 Shippingport, PA 15077 L-04-133 October 7, 2004 Beaver Valley Power Station Unit I - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73 | |||
------- -MonthiyOperatinigRcport U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen: | |||
In accordance with NRC Generic Letter 97-02, "Revised Contents of the Monthly Operating R Aeport", and Unit 1 and 2 Technical Specification 6.9.4, the "Monthly Operating Report" is' ubtnitted for Unit 1 and Unit 2 for the month of September, 2004. This information has alsb been inputted iinto the INPO Consolidated Data Entry (CDE) System. No regulatory commitments are 'contained in this submittal. | |||
Resp | |||
: tfully, L- | |||
: 1. W. Perc Vice-President BVPS DTJ/cmg Enclosures cc: | |||
NRC Regional 6fricef | |||
-;i o.PrussiaPA;;; | |||
;r' 9 -t y-- | |||
s i | |||
A | |||
.1 ;I-! | |||
rl | |||
OPERATING DATA REPORT DOCKET NO. | |||
UNIT NAME DATE COMPLETED BY TELEPHONE REPORTING PERIC 50-334 Beaver Valley 1 October 01. 2004 David T. Jones. | |||
(724) 682-4962 September 2004 | |||
: 1. Design Electrical Rating | |||
: 2. Maximum Dependable Capacity (MWe-Net) 835.00 821.00 | |||
: 3. | |||
Number of Hours the Reactor was Critical | |||
: 4. | |||
Number of Hours Generator On-line | |||
: 5. Reserve Shutdown Hours | |||
: 6. Net Electrical Energy Generated (MWHrs)_ | |||
This Month Yr-to-Date Cumulative 720.00 6,575.00 174,602.27 720.00 6,575.00 172,072.82 0.00 0.00 0.00 600,900.00 | |||
. 5,463,860.00 - 130,105,232.0 __. _ | |||
UNIT SHUTDOWNS | |||
.Type l | |||
Method of F: Forced Duration Shutting Cause & Corrective Action No. | |||
Date S: Scheduled (Hours) | |||
Reason 1 Down 2 Comments NONE. | |||
1 2 | |||
Reason: | |||
A Equipment Failure (Explain) | |||
B Maintenance or Test C | |||
Refueling D | |||
Regulatory Restriction E | |||
Operator Training & License Examination F | |||
Administration G | |||
Operational Error (Explain) | |||
H Other (Explain) | |||
Method: | |||
1 Manual 2 | |||
Manual Trip/Scram 3 | |||
Automatic Trip/Scram 4 | |||
Continuation 5 | |||
Other (Explain) | |||
==SUMMARY== | |||
: The Unit operated at a nominal value of 100% output for the entire month of September 2004. | |||
Page.1 of 1 | |||
OPERATING DATA REPORT DOCKET NO. | |||
50-412 UNIT NAME Beaver Valley 2 DATE October 01, 2004 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD: | |||
September 2004 | |||
: 1. | |||
Design Electrical Rating | |||
: 2. | |||
Maximum Dependable Capacity (MWe-Net) 836.00 831.00 This Month Yr-to-Date Cumulative | |||
: 3. | |||
Number of Hours the Reactor was Critical 720.00 6,575.00 124,183.48 | |||
: 4. | |||
Number of Hours Generator On-line 720.00 6,575.00 123,439.38 | |||
: 5. | |||
Reserve Shutdown Hours 0.00 0.00 0.00 | |||
_ 6.-Net Electrical.Energy.Generated (MWHrs) - | |||
594,967 00 5,452,717.00-97,272,115.00-UNIT SHUTDOWNS Type Method of F: Forced Duration Shutting Cause & Corrective Action No. | |||
Date S: Scheduled (Hours) | |||
Reason 1 Down 2 Comments NONE 1 | |||
Reason: | |||
A Equipment Failure (Explain) | |||
B Maintenance or Test C | |||
Refueling D | |||
Regulatory Restriction E | |||
Operator Training & License Examination F | |||
Administration G | |||
Operational Error (Explain) | |||
H Other (Explain) 2 Method: | |||
1 Manual 2 | |||
Manual Trip/Scram 3 | |||
Automatic Trip/Scram 4 | |||
Continuation 5 | |||
Other (Explain) | |||
==SUMMARY== | |||
: The Unit began the report period operating at a nominal value of 100% output.- On 9/9/04 at 0757 hours, -- | |||
the Unit reduced output by approximately 2% in order to gain extra margin as a conservative measure in order to prevent a possible Turbine runback or plant trip during the planned calibration of Loops 2 and 3 Delta-T/Tavg with Loop 1 experiencing fluctuations high. Following completion of the calibrations, the Unit was returned to full power at 0657 hours on 9/10/04. The Unit continued to operated at a nominal value of 100% output until 0928 hours on 9/24/04 when 2% load reduction was begun in order to lower Reactor power. Just prior to this, a level transient associated with the "B1 1 st Point Heater caused the isolation of extraction steam to the 2nd Point Heaters and a subsequent drop in feedwater temperature resulting in a Reactor power transient to approximately 100.8% output. | |||
Following an investigation into the cause for the Reactor power transient, the Unit subsequently reduced output to approximately 94% at 2057 hours on 9/24/04 in order to repack the pneumatic actuator for the Train B 1 st Point Heater Normal Level Control Valve. Following completion of repairs to the valve, the Unit commenced to return to full power at 0937 hours on 9/25/04. A nominal value of 100% output was achieved at 1218 hours on 9/25/04. The Unit continued to operate at a nominal value of 100% output for the remainder of the report period. | |||
Page 1 of 1}} | |||
Latest revision as of 00:39, 16 January 2025
| ML042940585 | |
| Person / Time | |
|---|---|
| Site: | Beaver Valley |
| Issue date: | 10/07/2004 |
| From: | Pearce L FirstEnergy Nuclear Operating Co |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| GL-97-002, L-04-133 | |
| Download: ML042940585 (3) | |
Text
&~rsrrayt Nclear Oper~q ap9y_
Beaver Valley Power Station P. 0. Box 4 Shippingport, PA 15077 L-04-133 October 7, 2004 Beaver Valley Power Station Unit I - Docket No. 50-334, License No. DPR-66 Unit 2 - Docket No. 50-412, License No. NPF-73
-MonthiyOperatinigRcport U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 Gentlemen:
In accordance with NRC Generic Letter 97-02, "Revised Contents of the Monthly Operating R Aeport", and Unit 1 and 2 Technical Specification 6.9.4, the "Monthly Operating Report" is' ubtnitted for Unit 1 and Unit 2 for the month of September, 2004. This information has alsb been inputted iinto the INPO Consolidated Data Entry (CDE) System. No regulatory commitments are 'contained in this submittal.
Resp
- tfully, L-
- 1. W. Perc Vice-President BVPS DTJ/cmg Enclosures cc:
NRC Regional 6fricef
-;i o.PrussiaPA;;;
- r' 9 -t y--
s i
A
.1 ;I-!
rl
OPERATING DATA REPORT DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE REPORTING PERIC 50-334 Beaver Valley 1 October 01. 2004 David T. Jones.
(724) 682-4962 September 2004
- 1. Design Electrical Rating
- 2. Maximum Dependable Capacity (MWe-Net) 835.00 821.00
- 3.
Number of Hours the Reactor was Critical
- 4.
Number of Hours Generator On-line
- 5. Reserve Shutdown Hours
- 6. Net Electrical Energy Generated (MWHrs)_
This Month Yr-to-Date Cumulative 720.00 6,575.00 174,602.27 720.00 6,575.00 172,072.82 0.00 0.00 0.00 600,900.00
. 5,463,860.00 - 130,105,232.0 __. _
UNIT SHUTDOWNS
.Type l
Method of F: Forced Duration Shutting Cause & Corrective Action No.
Date S: Scheduled (Hours)
Reason 1 Down 2 Comments NONE.
1 2
Reason:
A Equipment Failure (Explain)
B Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational Error (Explain)
H Other (Explain)
Method:
1 Manual 2
Manual Trip/Scram 3
Automatic Trip/Scram 4
Continuation 5
Other (Explain)
SUMMARY
- The Unit operated at a nominal value of 100% output for the entire month of September 2004.
Page.1 of 1
OPERATING DATA REPORT DOCKET NO.
50-412 UNIT NAME Beaver Valley 2 DATE October 01, 2004 COMPLETED BY David T. Jones TELEPHONE (724) 682-4962 REPORTING PERIOD:
September 2004
- 1.
Design Electrical Rating
- 2.
Maximum Dependable Capacity (MWe-Net) 836.00 831.00 This Month Yr-to-Date Cumulative
- 3.
Number of Hours the Reactor was Critical 720.00 6,575.00 124,183.48
- 4.
Number of Hours Generator On-line 720.00 6,575.00 123,439.38
- 5.
Reserve Shutdown Hours 0.00 0.00 0.00
_ 6.-Net Electrical.Energy.Generated (MWHrs) -
594,967 00 5,452,717.00-97,272,115.00-UNIT SHUTDOWNS Type Method of F: Forced Duration Shutting Cause & Corrective Action No.
Date S: Scheduled (Hours)
Reason 1 Down 2 Comments NONE 1
Reason:
A Equipment Failure (Explain)
B Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational Error (Explain)
H Other (Explain) 2 Method:
1 Manual 2
Manual Trip/Scram 3
Automatic Trip/Scram 4
Continuation 5
Other (Explain)
SUMMARY
- The Unit began the report period operating at a nominal value of 100% output.- On 9/9/04 at 0757 hours0.00876 days <br />0.21 hours <br />0.00125 weeks <br />2.880385e-4 months <br />, --
the Unit reduced output by approximately 2% in order to gain extra margin as a conservative measure in order to prevent a possible Turbine runback or plant trip during the planned calibration of Loops 2 and 3 Delta-T/Tavg with Loop 1 experiencing fluctuations high. Following completion of the calibrations, the Unit was returned to full power at 0657 hours0.0076 days <br />0.183 hours <br />0.00109 weeks <br />2.499885e-4 months <br /> on 9/10/04. The Unit continued to operated at a nominal value of 100% output until 0928 hours0.0107 days <br />0.258 hours <br />0.00153 weeks <br />3.53104e-4 months <br /> on 9/24/04 when 2% load reduction was begun in order to lower Reactor power. Just prior to this, a level transient associated with the "B1 1 st Point Heater caused the isolation of extraction steam to the 2nd Point Heaters and a subsequent drop in feedwater temperature resulting in a Reactor power transient to approximately 100.8% output.
Following an investigation into the cause for the Reactor power transient, the Unit subsequently reduced output to approximately 94% at 2057 hours0.0238 days <br />0.571 hours <br />0.0034 weeks <br />7.826885e-4 months <br /> on 9/24/04 in order to repack the pneumatic actuator for the Train B 1 st Point Heater Normal Level Control Valve. Following completion of repairs to the valve, the Unit commenced to return to full power at 0937 hours0.0108 days <br />0.26 hours <br />0.00155 weeks <br />3.565285e-4 months <br /> on 9/25/04. A nominal value of 100% output was achieved at 1218 hours0.0141 days <br />0.338 hours <br />0.00201 weeks <br />4.63449e-4 months <br /> on 9/25/04. The Unit continued to operate at a nominal value of 100% output for the remainder of the report period.
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