IR 05000456/2004007: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:October 29, 2004
 
==SUBJECT:==
BRAIDWOOD STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000456/2004007; 05000457/2004007
 
==Dear Mr. Crane:==
On September 30, 2004, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Braidwood Station, Units 1 and 2. The enclosed report documents the inspection findings which were discussed on September 30, 2004, with Mr. T. Joyce and other members of your staff.
 
The inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
Based on the results of this inspection, one NRC-identified finding of very low safety significance, which involved a violation of NRC requirements, was identified. However, because the violation was of very low safety significance and because the issue was entered into the licensees corrective action program, the NRC is treating the finding as a Non-Cited Violation in accordance with Section VI.A.1 of the NRCs Enforcement Policy. Additionally, a licensee-identified violation is listed in Section 4OA7 of this report.
 
If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -
Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Braidwood facility. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,
/RA/
Ann Marie Stone, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-456; 50-457 License Nos. NPF-72; NPF-77
 
===Enclosure:===
Inspection Report 05000456/2004007; 05000457/2004007 w/Attachment: Supplemental Information
 
REGION III==
Docket Nos:
50-456; 50-457 License Nos:
NPF-72; NPF-77 Report No:
05000456/2004007; 05000457/2004007 Licensee:
Exelon Generation Company, LLC Facility:
Braidwood Station, Units 1 and 2 Location:
35100 S. Route 53 Suite 79 Braceville, IL 60407-9617 Dates:
July 1 through September 30, 2004 Inspectors:
S. Ray, Senior Resident Inspector N. Shah, Resident Inspector L. Haeg, Reactor Engineer J. House, Senior Radiation Specialist H. Peterson, Senior Operations Engineer R. Skokowski, Senior Resident Inspector, Byron Station P. Snyder, Resident Inspector, Byron Station T. Tongue, Project Engineer P. Smith, Illinois Emergency Management Agency Observers:
S. Cameron, Student Engineer J. Robbins, Reactor Engineer A. Wichman, Student Engineer M. Wilke, Reactor Engineer Approved by:
Ann Marie Stone, Chief Branch 3 Division of Reactor Projects
 
Enclosure
 
=SUMMARY OF FINDINGS=
IR 05000456/2004007, 05000457/2004007; 07/01/04 - 09/30/04; Braidwood Station,
 
Units 1 & 2; Post-Maintenance and Surveillance Testing.
 
This report covers a 3-month period of baseline resident inspection and an announced baseline inspection on radiation protection. The inspection was conducted by Region III inspectors and the resident inspectors. One Green finding associated with a Non-Cited Violation was identified. The significance of most findings is indicated by their color (Green, White, Yellow,
Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,
Revision 3, dated July 2000.
 
A.
 
Inspector-Identified and Self-Revealed Findings
 
===Cornerstone: Barrier Integrity===
*
: '''Green.'''
The inspectors identified a finding of very low safety significance when they noted that the procedures for operating the hydrogen recombiners, if followed as written, would have resulted in the recombiners operating at too low of a temperature to be effective. This was due to a revision that changed the startup procedure, but not the panel lineup and shutdown procedures. The causes of this violation were related to the cross-cutting areas of Human Performance, because a system engineer failed to properly revise the procedures, and Problem Identification and Resolution, because the purpose of the revision was as a corrective action for a previously identified violation and was not effective. The condition existed for a period of 2 weeks before being identified and corrected through another procedure revision.
 
The finding was more than minor because it affected the Barrier Integrity cornerstone objective of providing reasonable assurance that the physical containment barrier would protect the public from radio nuclide releases caused by accidents or events. The finding was of very low safety significance because the hydrogen recombiner system is not a significant contributor to the large early release frequency for pressurized water reactors with large dry containments. This issue was determined to be a non-cited violation of 10 CFR 50, Appendix B, Criteria V, for procedures that were not appropriate to the circumstances. (Section 1RST)
 
===Licensee-Identified Violations===
A violation of very low safety significance, which was identified by the licensee as been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and the licensees corrective action tracking number is listed in Section 4OA7 of this report.
 
=REPORT DETAILS=
 
===Summary of Plant Status===
Unit 1 operated at or near full power for the entire inspection period except that power was reduced to about 88 percent from July 4 through July 6, 2004, for turbine and governor valve testing. On about September 27 the licensee began a gradual coastdown of power in preparation for a refueling outage. Power had been reduced to about 95 percent at the end of the inspection period.
 
Unit 2 operated at or near full power for the entire inspection period except that power was reduced to 86 percent on September 27 for turbine and governor valve testing.
 
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R04}}
 
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
 
===.1 Complete Walkdowns===
====a. Inspection Scope====
The inspectors performed a complete system walkdown of the Unit 2 safety injection system. This walkdown represented one inspection sample. This system was selected because it emergency core cooling system (ECCS) valves were a moderately high contributor to the overall core damage frequency in the licensees probabilistic risk analysis.
 
In addition to the walkdown, the inspectors reviewed the following:
* selected operating, emergency, and surveillance procedures which involved manipulations of safety injection valves;
* the Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS), and other selected design bases documentation regarding the safety injection system;
* condition reports (CRs) for the system initiated within the last year; and
* outstanding system work orders (WOs).
 
The inspectors also reviewed the CRs to determine whether issues were being properly addressed in the licensees corrective actions program. Documents reviewed as part of this inspection are listed in the Attachment.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Partial Walkdowns===
====a. Inspection Scope====
The inspectors performed partial walkdowns of the accessible portions of risk-significant system trains during periods when the train was of increased importance due to redundant trains or other equipment being unavailable. The inspectors utilized the valve and electric breaker checklists, as well as other documents listed in the Attachment, to determine that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to confirm there were no obvious deficiencies. The inspectors reviewed outstanding WOs and CRs associated with the train to determine whether those documents revealed issues that could affect train function. The inspectors used the information in the appropriate sections of the TS and the UFSAR to determine the functional requirements of the system. The inspectors also reviewed the licensees identification of and the controls over the redundant risk-related equipment required to remain in service. The inspectors completed four samples of this requirement by walkdowns of the following trains:
* the 1B centrifugal charging system prior to planned maintenance on the 1A chemical and volume control train;
* the 1A residual heat removal (RH) train prior to a planned work window on the 1B RH train;
* the 2B emergency diesel generator (DG) prior to a planned work window on the 2A DG; and
* the 1B essential service water pump during a planned work window on the 1A pump.
 
====b. Findings====
No findings of significance were identified. {{a|1R05}}
 
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
Quarterly Area Walkdowns
 
====a. Inspection Scope====
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles and ignition sources, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events with later additional insights or their potential to impact equipment which could initiate a plant transient. The inspectors used the documents listed in the to determine whether fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action program.
 
The inspectors completed ten samples of this inspection requirements during the following walkdowns:
* main control room (Fire Zone 2.1-0);
* division 12 engineered safety feature (ESF) switchgear room (Fire Zone 5.1-1);
* division 11 ESF switchgear room (Fire Zone 5.2-1);
* division 22 ESF switchgear room (Fire Zone 5.1-2);
* division 21 ESF switchgear room (Fire Zone 5.2-2);
* turbine building 451 foot elevation (Fire Zone 8.6-0);
* turbine building 369 foot elevation Unit 1 (Fire Zones 8.1-0 and 8.2-1);
* technical support center (Fire Zone 18.26-1);
* 1B DG room (Fire Zone 9.1-1); and
* turbine building 369 foot elevation Unit 2 (Fire Zone 8.2-2).
 
====b. Findings====
No findings of significance were identified. {{a|1R11}}
 
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11}}
 
===.1 Quarterly Review of Testing/Training Activity===
====a. Inspection Scope====
The inspectors observed an operating crew performance during an evaluated simulator out-of-the-box scenario. The inspectors evaluated crew performance in the following areas:
* clarity and formality of communications;
* ability to take timely actions in the safe direction;
* prioritization, interpretation, and verification of alarms;
* procedure use;
* control board manipulations;
* oversight and direction from supervisors; and
* group dynamics.
 
Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the Exelon procedures listed in the Attachment.
 
The inspectors confirmed that the crew completed the critical tasks listed in the simulator guide. The inspectors also compared simulator configurations with actual control board configurations. For any weaknesses identified, the inspectors observed the licensee evaluators to determine whether they also noted the issues and discussed them in the critique at the end of the session. This inspection constituted one sample.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Biennial Written Examination and Annual Operating Test Results===
====a. Inspection Scope====
The inspectors reviewed the overall pass/fail results of individual Job Performance Measure (JPM) operating tests, and simulator operating tests (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee during calender year 2004. A written examination was conducted; however, it was not considered or taken credit for as the NRC comprehensive biennial examination. The overall results were compared with the significance determination process in accordance with NRC Manual Chapter 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process (SDP).
 
====b. Findings====
No findings of significance were identified. {{a|1R12}}
 
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
Routine Inspection
 
====a. Inspection Scope====
The inspectors reviewed the licensees overall maintenance effectiveness for risk-significant event initiating, mitigating, and barrier integrity systems. This evaluation consisted of the following specific activities:
* observing the conduct of planned and emergent maintenance activities where possible;
* reviewing selected CRs, open WOs, and control room log entries in order to identify system deficiencies;
* reviewing licensee system monitoring and trend reports;
* attending various meetings throughout the inspection period where the status of maintenance rule activities was discussed;
* a partial walkdown of the selected system; and
* interviews with the appropriate system engineer.
 
The inspectors also reviewed whether the licensee properly implemented the Maintenance Rule, 10 CFR 50.65, for the system. Specifically, the inspectors determined whether:
* the system was scoped in accordance with 10 CFR 50.65;
* performance problems constituted maintenance rule functional failures;
* the system had been assigned the proper safety significance classification;
* the system was properly classified as (a)(1) or (a)(2); and
* the goals and corrective actions for the system were appropriate.
 
The above aspects were evaluated using the maintenance rule program and other documents listed in the Attachment. The inspectors also confirmed that the licensee was appropriately tracking reliability and/or unavailability for the systems.
 
The inspectors completed three samples in this inspection requirement by reviewing the following systems:
* instrument power;
* ground detection and cathodic protection system, and
* emergency DGs.
 
====b. Findings====
No findings of significance were identified. {{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
 
====a. Inspection Scope====
The inspectors reviewed the licensees management of plant risk during emergent maintenance activities or during activities where more than one significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety-significant equipment. The inspections were conducted to determine whether evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and that contingency plans were in place where appropriate.
 
The licensees daily configuration risk assessments records, observations of operator turnover and plan-of-the-day meetings, observations of work in progress, and the documents listed in the Attachment were used by the inspectors to determine whether the equipment configurations were properly listed, that protected equipment were identified and were being controlled where appropriate, that work was being conducted properly, and that significant aspects of plant risk were being communicated to the necessary personnel. The inspectors confirmed that the licensee controlled emergent work in accordance with the expectations in the procedures listed in the Attachment.
 
In addition, the inspectors reviewed selected issues that the licensee entered into its corrective action program to determine whether identified problems were being entered into the program with the appropriate characterization and significance. The inspectors confirmed that minor issues identified during these inspections were entered into the licensee corrective action program.
 
The inspectors completed six samples by reviewing the following activities:
* cleaning and testing of both trains of Unit 1 reactor containment fan coolers (RCFCs) following identification of low service water flow from fouling followed by thermal performance testing of the Unit 2 RCFCs;
* operator response following an unplanned urgent failure of the Unit 1 rod control system;
* operator response following an unplanned loss of the Unit 1 containment high-3 pressure sensing relay;
* identification of low service water flow on the 2B RCFC during planned maintenance on the 2A DG and 2B component cooling (CC) pump;
* an emergent issue with switchyard breaker 1-8 during planned maintenance on the 2B CC pump; and
* planned maintenance on battery charger 211 requiring direct current (DC) cross-tie from Unit 2 DC bus 211 to Unit 1 DC bus 111.
 
====b. Findings====
No findings of significance were identified. {{a|1R14}}
 
==1R14 Operator Performance During Non-Routine Evolutions and Events==
{{IP sample|IP=IP 71111.14}}
 
====a. Inspection Scope====
The inspectors completed one sample by observing the following event:
* an unplanned entry into 0BwOA Elec-1, Abnormal Grid Conditions-Unit 0, after the licensee was notified by the Transmissions Group of potential, degraded voltage conditions in the Units 1 and 2 switchyard.
 
For this event, the inspectors interviewed plant operators and reviewed plant records including control room logs, operator turnovers, and CRs. The inspectors confirmed that the control room response was consistent with 0BwOA Elec-1 and determined whether identified discrepancies were captured in the corrective action program.
 
Documents reviewed as part of this inspection are listed in the Attachment.
 
====b. Findings====
No findings of significance were identified. {{a|1R15}}
 
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15}}
 
====a. Inspection Scope====
The inspectors evaluated plant conditions and selected CRs for risk-significant components and systems in which operability issues were questioned. These conditions were evaluated to determine whether the operability of components was justified. The inspectors compared the operability and design criteria in the appropriate section of the UFSAR to the licensees evaluations presented in the CRs and documents listed in the Attachment to determine whether the components or systems were operable. The inspectors also conducted interviews with the appropriate licensee system engineers and conducted plant walkdowns, as necessary, to obtain further information regarding operability questions. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action program.
 
The inspectors completed eight samples by reviewing the following operability evaluations and conditions:
* Unit 1 rod control system following an unplanned rod control urgent failure alarm;
* S hooks on electro-thermal links for fire dampers installed incorrectly;
* Unit 1 and 2 lightning arrester system following several Unit 1 rod urgent failure alarms due to lightning strikes;
* 2D RCFC flow instrument not responding;
* low service water flow to the 2B RCFC;
* adequacy of TS 3.6.6 for containment spray and cooling systems;
* failure of Instrument Inverter 114; and
* discolored oil on the 2B CC pump outer bearing.
 
====b. Findings====
No findings of significance were identified. {{a|1R17}}
 
==1R17 Permanent Plant Modifications==
{{IP sample|IP=IP 71111.17}}
Annual Review
 
====a. Inspection Scope====
The inspectors evaluated the permanent plant modification installed under Engineering Change Request 348152 to relocate the sample lines for control room radiation monitors 0PR31J, 0PR32J and 0PR33J. This modification affected a safety-significant barrier integrity system and was one of the corrective actions in response to Licensee Event Report (LER) 2003-001-00, Control Room Ventilation System Alignment Results in Inoperable Radiation Monitors.
 
The inspectors reviewed the design change package and associated work orders for installation and observed the pre-job brief and actual installation of the modification.
 
After the modification was installed, the inspectors performed a walkdown of the radiation monitors to determine whether operation was proper. The inspectors confirmed that the modification did not introduce any new system vulnerabilities and did not create any new system interface problems. Documents reviewed as part of this inspection are listed in the Attachment. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action system.
 
This activity constituted one inspection sample of the annual requirement.
 
====b. Findings====
No findings of significance were identified.
1RST Post-Maintenance and Surveillance Testing - Pilot (71111.ST)
 
====a. Inspection Scope====
The inspectors reviewed post-maintenance and surveillance testing activities associated with important mitigating, barrier integrity, and support systems to ensure that the testing adequately demonstrated system operability and functional capability. For post-maintenance testing, the inspectors used the appropriate sections of the TS and UFSAR, as well as the WOs for the work performed, to evaluate the scope of the maintenance and to determine whether the post-maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. For surveillance testing, the inspectors determined whether the testing met the TS, the UFSAR, and licensee procedural requirements, and demonstrated that the equipment was capable of performing its intended safety functions. The inspectors determined whether the testing met the frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria was met; and that the results of the tests were properly reviewed and recorded. The activities were selected based on their importance in demonstrating mitigating systems capability and barrier integrity. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action program. Documents reviewed as part of this inspection are listed in the Attachment.
 
Note that this inspection is a pilot for a proposed consolidated procedure combining the previous Post-Maintenance Testing (71111.19) and Surveillance Testing (71111.22)procedures.
 
Five samples were completed by observing post-maintenance testing after the following activities:
* procedure revisions and annunciator repair on the 0A hydrogen recombiner;
* planned maintenance of the 1A centrifugal charging pump;
* planned maintenance on the 1B RH train;
* planned maintenance on the 2A DG; and
* emergent bearing change on the 2B CC pump.
 
Four samples were completed by observing and evaluating the following surveillance tests:
* Unit 1 motor-driven auxiliary feedwater pump quarterly;
* local leak rate testing of the of the Unit 1 containment miniflow purge isolation valves;
* new fuel receipt and inspections; and
* Unit 2 reactor containment fan coolers monthly surveillance testing.
 
====b. Findings====
=====Introduction:=====
The inspectors identified a Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criteria V, having a very low safety significance (Green) for an inadequate procedure for startup of the hydrogen recombiners. The procedure, if followed as written, would have resulted in the recombiners operating at too low of a temperature to be effective.
 
=====Description:=====
As a result of one of the issues associated with a finding discussed in Inspection Report 05000456/2004004; 05000457/2004004, Section 1R15.1, the licensee revised the procedure for startup of the hydrogen recombiners (BwOP OG-10)on July 9, 2004. The revision removed the steps calling for manual adjustment of the reaction chamber gas temperature controller during startup to let the recombiner come up to the normal operating temperature of 1325 degrees Fahrenheit automatically as described in the UFSAR.
 
On July 23, 2004, the inspectors attended a pre-job briefing for a planned startup of the 0A hydrogen recombiner. The system engineer had proposed to demonstrate that the recombiner would operate properly with the revised procedure. During the briefing, an operator noted that the first step of the startup procedure required completion of the recombiner panel lineup sheet (BwOP OG-10T1). The panel lineup sheet called for the reaction chamber gas temperature controller to be set at 1100 degrees Fahrenheit and the operator questioned whether that was the correct value. The inspectors informed the operators that it appeared that the panel lineup sheet had not been revised when the startup procedure was revised. The inspectors also noted that the recombiner shutdown procedure (BwOP OG-9) also called for leaving the temperature controller set to 1100 degrees when the system was shutdown.
 
The work execution center supervisor called the system engineer who confirmed that both procedures should have been revised to list 1325 degrees, the normal recombiner operating temperature, instead of 1100 degrees. The system engineer stated that he had not realized that the panel lineup and shutdown procedures needed to be changed at the same time that the startup procedure was revised. The licensee revised both procedures to include the correct 1325 degree setpoint later on July 23, 2004, and the 0A recombiner was started up and operated.
 
=====Analysis:=====
The inspectors determined that failure to revise the panel lineup and shutdown procedures was a performance deficiency warranting a significance evaluation. Had a hydrogen recombiner been needed for an event between July 9 and July 23, 2004, and operators had followed the procedures as written, the recombiner reaction chamber gas temperature would have controlled at 1100 degrees rather than the 1325 degrees necessary for a proper oxygen/hydrogen recombination reaction. The same common procedure was used for both trains of recombiners so neither would have functioned properly in an event. The inspectors concluded that the finding was greater than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued on June 20, 2003. The inspectors answered yes to minor Question Number 4 because the finding was associated with the containment Barrier Integrity cornerstone attribute of risk important systems function and affected the cornerstone objective of providing reasonable assurance that the physical containment barrier would protect the public from radio nuclide releases caused by accidents or events. The function of the recombiners was to remove hydrogen from the containment, post accident, before it threatened containment integrity by reaching highly flammable concentrations. The finding also affected the cross-cutting areas of Human Performance, because the system engineer failed to revise two necessary procedures, and Problem Identification and Resolution, because the corrective action for the violation discussed in the previously mentioned inspection report was not adequately implemented.
 
The inspectors completed a significance determination of this issue using IMC 0609, Significance Determination Process, dated March 21, 2003. Using the Phase 1 screening worksheet in Appendix A, Attachment 1, dated September 10, 2004, the inspectors answered yes to Question 3 in the Containment Barriers column because the finding caused an actual reduction in defense-in-depth for the hydrogen control function of the reactor containment. The inspectors conducted a Phase 2 analysis using IMC 0609 Appendix H, Containment Integrity Significance Determination Process, dated May 6, 2004. The finding was screened as Green because it did not affect the core damage frequency and inoperability of the hydrogen recombiner did not have a significant effect on the large early release frequency for a pressurized water reactor with a large dry containment. In addition, the inspectors determined through discussions with operators and engineers, as well as observations of the emergency response organization, that the procedure discrepancies would probably have been identified and corrected in an actual event. Therefore, this finding was considered to be of very low safety significance (Green) and was assigned to the Barrier Integrity cornerstone of both units.
 
=====Enforcement:=====
Criterion V, Instructions, Procedures, and Drawings, of 10 CFR 50, Appendix B required, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Contrary to the above, between July 9 and July 23, 2004, the procedures for operating the hydrogen recombiners were not appropriate because they would have resulted in the recombiners operating at too low a temperature to be effective. The procedures were revised on July 23, 2004, and demonstrated to be appropriate. The licensee entered the issue into its corrective action program as CR 238380. Because this violation was of very low safety significance and it was entered into the licensees corrective action program, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy.
 
(NCV 05000456/2004007-01; 05000457/2004007-01)
{{a|1R23}}
 
==1R23 Temporary Plant Modifications==
{{IP sample|IP=IP 71111.23}}
 
====a. Inspection Scope====
The inspectors reviewed the current status of the Units 1 and 2 positive displacement pumps. These pumps were originally installed equipment that were not being used or maintained by the licensee, but which had not been officially classified as abandoned.
 
The positive displacement pumps were not considered safety-related, but did interface with the refueling water storage tank, a safety-related component, and were considered a backup pump to the safety-related centrifugal charging pumps. The inspectors determined that the change did not have an unanalyzed affect on the safety functions of important safety systems. As part of this inspection, the inspectors reviewed the 10 CFR 50.59 screening, appropriate UFSAR sections, and the TS, to determine whether system operability/availability was affected. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action program. Documents reviewed as part of this inspection are listed in the
. This review constituted one sample of this inspection requirement.
 
====b. Findings====
No findings of significance were identified.
 
===Cornerstone: Emergency Preparedness===
{{a|1EP6}}
 
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06}}
 
====a. Inspection Scope====
The inspectors observed licensee performance during an evaluated emergency response drill. Observations included manning of the Technical Support Center (TSC),turnover of command and control to and from the TSC, event classification and notification, and development of protective action recommendations. The inspectors also observed Operations Support Center (OSC) activities and accompanied one in-plant team. The inspectors confirmed that deficiencies noted during the drill, by either the inspectors or licensee evaluators, were entered into the licensees corrective action program. The inspectors also attended portions of the post drill critique for the TSC and OSC crews. Documents reviewed as part of this inspection are listed in the Attachment.
 
This activity constituted one inspection sample.
 
====b. Findings====
No findings of significance were identified.
 
==RADIATION SAFETY==
===Cornerstone: Public Radiation Safety===
2PS2 Radioactive Material Processing and Transportation (71122.02) Shipment Preparation
 
====a. Inspection Scope====
The inspectors reviewed shipment packaging and surveying, emergency instructions, disposal manifest, and shipping papers provided to the driver. The receiving licensees authorization to receive the shipment package was verified. Radiation worker practices were observed in order to verify that the workers had adequate skills to accomplish each task and to determine if the shippers were knowledgeable of the shipping regulations and whether shipping personnel demonstrated adequate skills to accomplish the package preparation requirements for public transport with respect to NRC Bulletin 79-19 and 49 CFR Part 172 Subpart H. The review was conducted to verify that the licensees training program provided training consistent with NRC and Department of Transportation requirements. These reviews represented one sample.
 
====b. Findings====
No findings of significance were identified.
 
==OTHER ACTIVITIES==
Cornerstones: Mitigating Systems and Barrier Integrity {{a|4OA1}}
 
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
Reactor Safety Strategic Area
 
====a. Inspection Scope====
The inspectors reviewed the documents listed in the Attachment to determine whether the licensee had corrected reported performance indicator data, in accordance with the criteria in NEI [Nuclear Energy Institute] 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 2. The data reported by the licensee was compared to a sampling of control room logs, CRs, and other sources of data generated since the last verification. The inspectors determined that minor issues identified during the inspection were entered into the licensees corrective action program. The inspectors completed six samples by examining the following performance indicators:
Unit 1
* safety system unavailability - auxiliary feedwater system for the period of July 1, 2003 through June 30, 2004;
* safety system functional failures for the period of July 1, 2003 through June 30, 2004; and
* reactor coolant system activity for the period of May 1, 2003 through June 30, 2004.
 
Unit 2
* safety system unavailability - auxiliary feedwater system for the period of July 1, 2003 through June 30, 2004;
* safety system functional failures for the period of July 1, 2003 through June 30, 2004; and
* reactor coolant system activity for the period of May 1, 2003 through June 30, 2004.
 
====b. Findings====
No findings of significance were identified. {{a|4OA2}}
 
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152}}
 
===.1 Routine Review of Identification and Resolution of Problems===
====a. Inspection Scope====
As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to determine whether they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Minor issues entered into the licensees corrective action program as a result of the inspectors observations are generally denoted in the Attachment. These activities were part of normal inspection activities and were not considered separate samples.
 
====b. Findings====
No finding of significance were identified.
 
===.2 Boric Acid Leakage Identification and Resolution (Annual Sample)===
Introduction The inspectors reviewed the licensees process for identifying and resolving borated water leaks. The inspection focused on how identified leakage was being identified, how it was documented and tracked, and what corrective actions were taken. The inspectors were particularly concerned with how the licensee addressed those components particularly susceptible to boric acid corrosion. This inspection was prompted by an apparent increasing trend in the number of borated water leaks the licensee had identified over the past year. Additionally, this inspection was also planned to review the effectiveness of the licensees new boric acid control program, which was implemented in August 2003. As a guide in this program, the inspectors referred to the Electric Power and Research Institute document No. 1000975, Boric Acid Corrosion Guidebook, Revision 1.
 
a.
 
Effectiveness of Problem Identification
: (1) Inspection Scope The inspectors reviewed those station procedures implementing the licensees boric acid control program. The inspectors also reviewed the CRs listed in the Attachment to determine whether borated water leaks were being properly identified and evaluated.
 
The inspectors performed walkdowns of selected areas of the auxiliary building to observe boric acid leakage and conducted interviews with selected licensee staff to determine whether the boric acid program requirements were understood.
: (2) Issues The licensees procedures required that boric acid leakage be documented in CRs and routed to the station Boric Acid Control Coordinator (BACC) for review. The BACC was responsible for tracking, evaluating and resolving boric acid leaks. The inspectors noted that the procedures were consistent with the aforementioned industry document including identifying specific components and systems susceptible to boric acid corrosion.
 
During interviews, the BACC stated that the increase in CRs resulted from a renewed emphasis on identifying and resolving boric acid leakage following the implementation of the new program and in light of recent industry lessons learned. This resulted in more frequent plant walkdowns by the BACC and an increased awareness among plant staff following supplemental training on the new program requirements.
 
The inspectors observed that the majority of the boric acid CRs generated over the past year were written by the BACC. There were some CRs generated by the other work groups, primarily radiation protection and operations staff, however, the BACC stated that most boric acid issues were verbally communicated to him. The BACC maintained a database of all identified leaks tracking, in part, the date of identification, current status and planned corrective actions.
 
During plant walkdowns, the inspectors noted that most observed leaks were recorded in the BACC database. Those leaks identified by the inspectors, but not in the database, were documented in CRs by the BACC. The inspectors also noted that, when interviewed, licensee staff generally understood the boric acid program requirements.
 
However, the inspectors identified some instances where leaks from borated water systems were documented in CRs, but were not sent to the BACC for review. The specific examples did not affect the operability of safety-significant systems, but did indicate a possible lack of sensitivity to boric acid leakage during the licensees CR review process. The BACC documented this issue in a CR for followup.
 
b.
 
Effectiveness of Corrective Actions
: (1) Inspection Scope The inspectors reviewed CRs documenting boric acid leakage and the BACC database to determine whether the licensee was effectively addressing boric acid leakage concerns. Specifically, for selected issues, the inspectors reviewed the as found reports, the associated engineering evaluation, the proposed corrective actions and interviewed licensee personnel. As part of this review, the inspectors performed plant walkdowns to observe the condition of the repaired components.
: (2) Issues The licensee appeared to be properly evaluating and correcting boric acid leaks.
 
Specifically, the inspectors noted that the evaluations identified the source and nature of the deposits, the operability of the affected components, whether the leakage was recurring, the planned corrective actions and, if the issue had been resolved, whether the corrective actions were effective. There was also reasonable and sufficient documentation for each issue.
 
The corrective actions for the reviewed items appeared adequate, were focused on the apparent cause for each condition and were appropriately scheduled for timeliness. The inspectors observed that active leaks having interim corrective actions, but not yet repaired, were contained and that there was no apparent further component degradation. For those leaks considered permanently repaired, the inspectors observed no recurrence of leakage.
{{a|4OA3}}
 
==4OA3 Event Followup==
{{IP sample|IP=IP 71153}}
The inspectors completed four inspection samples in this area.
 
===.1 Licensee Event Report Review===
a.
 
(Closed) LER 05000456/2004-002-00: 1C Reactor Containment Fan Cooler Discovered to be Inoperable Greater Than Required TS Allowed Outage Time On June 1, 2004, during a monthly surveillance test, the licensee discovered that the essential service water flow rate through the 1C RCFC was below the limit of 2660 gallons per minute (gpm) of TS 3.6.6. The licensees investigation determined that the flow had been below the TS limit since May 6, 2004, a period longer than the 7-day allowed outage time of the TS. The flow had been set too low in May due to the fact that the flow indication was inaccurate due to partial blocking from calcium carbonate deposits. Corrective actions, as discussed in the LER and in CR 224989, included cleaning and calibrating the flow detectors of all the RCFCs, resetting the flow control throttling valve for the 1C RCFC, and strengthening the program for creating and implementing adverse condition monitoring plans.
 
The inspectors concluded that the issue was greater than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued on June 20, 2003. The inspectors answered yes to minor Question Number 4 because the finding was associated with the containment Barrier Integrity cornerstone attribute of risk important systems function and affected the cornerstone objective of providing reasonable assurance that the physical containment barrier would protect the public from radio nuclide releases caused by accidents or events. The function of the RCFCs was to remove heat to limit the post-accident pressure in the containment.
 
The inspectors completed a significance determination of this issue using IMC 0609, Significance Determination Process, dated March 21, 2003. Using the Phase 1 screening worksheet in Appendix A, Attachment A, dated September 10, 2004, the inspectors answered yes to Question 3 in the Containment Barriers column because the finding caused an actual reduction in defense-in-depth for the atmospheric pressure control function of the reactor containment. The inspectors conducted a Phase 2 analysis using IMC 0609 Appendix H, Containment Integrity Significance Determination Process, dated May 6, 2004. The finding was screened as Green because it did not affect the core damage frequency and inoperability of an RCFC did not have a significant effect on the large early release frequency for a pressurized water reactor with a large dry containment. In addition, as discussed in the LER, based on the actual essential service water temperature during the period of inoperability, there was only a short period of time where even the degraded train of RCFCs alone would not have been able to perform its safety function. Therefore, this finding was considered to be of very low safety significance (Green) and was assigned to the Barrier Integrity cornerstone of Unit 1.
 
This licensee-identified finding involved a violation of TS 3.6.6, Containment Spray and Cooling Systems. The enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.
 
b.
 
(Closed) LER 05000456/2004-003-00: 0A Hydrogen Recombiner Identified to be Inoperable Greater Than the Required TS Allowed Outage Time On June 16, 2004, the licensee identified that the 0A hydrogen recombiner had been inoperable in excess of the 30 day Allowed Outage Time permitted by TS 3.6.8.
 
Specifically, the recombiner had been inoperable since March 3, 2004, when the heater breaker tripped during post-maintenance testing. This issue was previously considered a Non-Cited Violation and a finding of very low safety significance (Green). This issue was assigned to the Barrier Integrity cornerstone of both units since the 0A recombiner could serve either unit. The specifics of the issue including the inspectors review and significance determination were discussed in NRC Inspection Report 05000456/2004004; 05000457/2004004. This LER is closed.
 
===.2 Notification of Loss of Emergency Preparedness Capabilities===
On August 4, 2004, the licensee notified the NRC via the Emergency Notification System, that it had experienced a major loss of emergency preparedness capabilities.
 
Due to lightening and severe weather the night of August 3-4, 2004, the licensee experienced short periods where more than 25 percent of their offsite notification sirens were inoperable. The longest period was for about 42 minutes. The inspectors reviewed the records and determined that the public notification capabilities were restored in a timely manner and that the problem had been entered into the licensees corrective action program. This issue was not a violation of NRC requirements.
 
===.3 Increase in Unit 1 Containment Noble Gas Levels===
====a. Inspection Scope====
On August 5, 2004, the licensee recognized an increase in Unit 1 containment noble gas levels, which indicated a small reactor coolant system leak. The leak was so small that there was no discernable increase in the leak rate calculation performed. On August 9, 2004, licensee personnel completed a containment tour and identified a small steam leak at a fitting on the pressurizer steam space sample line. Although the sample line was isolated, it appeared that the isolation valve (1PS9350A) was leaking by. The licensee evaluated the leak rate and the impact of the leak with no significant concerns identified. On August 12, 2004, the licensee performed another containment entry and closed a manual isolation upstream of the leak and effectively stopped the leak.
 
From the time the licensee identified the increase in noble gases, until the licensee stopped the leak on August 12, 2004, the inspectors monitored the leak rate, and the licensees performance to address the concern. This included accompanying licensee personnel during the containment entry on August 12, 2004. The inspectors confirmed that the leak rate levels never approached the TS limits. Also, the inspectors assess the leak-by associated with the isolation valve 1PS9350A and confirmed that the condition was not prohibited by TS. Documents reviewed as part of this inspection were listed in the Attachment.
 
====b. Findings====
No findings of significance were identified.
 
===.4 Notification of a Minor Oil Spill===
On September 13, 2004, the licensee notified the NRC via the Emergency Notification System that it had notified the appropriate agencies of a small hydraulic oil spill on the property adjacent to the station. The inspectors determined that the event was not a significant NRC regulatory concern and did no followup. This activity was not considered an inspection sample but was included in the report to complete the public record.
 
{{a|4OA4}}
 
==4OA4 Cross-Cutting Aspects of Findings==
===.1 The finding described in Section 1RST of this report had, as one of its causes, a human===
performance deficiency, in that, the system engineer failed to revise two other applicable procedures when revising the startup procedure for the hydrogen recombiners, resulting in procedures that would not have worked if called upon.
 
===.2 The finding described in Section 1RST of this report also had, as another one of its===
causes, a problem identification and resolution deficiency, in that, the licensee corrective actions following a previously identified violation for the hydrogen recombiners were not effective.
 
{{a|4OA5}}
 
==4OA5 Other Activities==
Review of Institute of Nuclear Power Operations Report The inspectors completed a review of the final report for the Institute of Nuclear Power Operations, January 2004 Evaluation, dated July 23, 2004.
 
{{a|4OA6}}
 
==4OA6 Meetings==
Exit Meeting The inspectors presented the inspection results to Mr. T. Joyce and other members of licensee management at the conclusion of the inspection on September 30, 2004. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
 
{{a|4OA7}}
 
==4OA7 Licensee-Identified Violations==
The following violations of very low safety significance were identified by the licensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Manual, NUREG-1600, for being dispositioned as NCVs.
 
===Cornerstone: Barrier Integrity===
Technical Specification 3.6.6 required that two containment spray trains and two containment cooling trains shall be operable in Modes 1, 2, 3, and 4. With one or more containment cooling trains inoperable the trains must be restored to operable within 7 days or the unit be placed in Mode 3 within 6 hours. Surveillance Requirement 3.6.6.3 for demonstrating operability of the containment cooling train required that cooling water flow rate be greater than or equal to 2660 gpm. As described in LER 05000456/2004-002-00 and Section 4OA3.1a of this report, between May 6, 2004, and June 1, 2004, the cooling water flow to the 1C RCFC was less than 2660 gpm. The licensee entered this issue into its corrective action program as CR 224989.
 
ATTACHMENT:
 
=SUPPLEMENTAL INFORMATION=
 
==KEY POINTS OF CONTACT==
Licensee
: [[contact::T. Joyce]], Site Vice President
: [[contact::K. Polson]], Plant Manager
: [[contact::D. Ambler]], Regulatory Assurance Manager
: [[contact::D. Burton]], Licensed Operator Requalification Training Group Lead
: [[contact::S. Butler]], Regulatory Assurance - NRC Coordinator
: [[contact::G. Dudek]], Operations Director
: [[contact::R. Gilbert]], Nuclear Oversight Manager
: [[contact::J. Kuczynski]], Chemistry Manager
: [[contact::D. Morse]], Radioactive Materials Shipper
: [[contact::J. Moser]], Radiation Protection Manager
: [[contact::M. Smith]], Engineering Director
: [[contact::E. Wrigley]], Maintenance Director
Nuclear Regulatory Commission
: [[contact::A. Stone]], Chief, Reactor Projects Branch 3
 
==LIST OF ITEMS==
===OPENED, CLOSED AND DISCUSSED===
===Opened===
: 05000456/2004007-01;
: 05000457/2004007-01 NCV Failure to Have Appropriate Procedures for Operation of the Hydrogen Recombiners (Section 1RST)
 
===Closed===
: 05000456/2004007-01;
: 05000457/2004007-01 NCV Failure to Have Appropriate Procedures for Operation of the Hydrogen Recombiners (Section 1RST)
: 05000456/2004-002-00 LER 1C Reactor Containment Fan Cooler Discovered to be Inoperable Greater Than Required TS Allowed Outage Time (Section 4OA3.1a)
: 05000456/2004-003-00 LER 0A Hydrogen Recombiner Identified to be Inoperable Greater Than the Required TS Allowed Outage Time (Section 4OA3.1b)
 
===Discussed===
None.
 
==LIST OF DOCUMENTS REVIEWED==
 
}}
}}

Latest revision as of 23:58, 15 January 2025

IR 05000456-04-007, 05000457-04-007; on 07/01/2004 - 09/30/2004; Braidwood Station, Units 1 and 2; Post-Maintenance and Surveillance Testing
ML043060332
Person / Time
Site: Braidwood  Constellation icon.png
Issue date: 10/29/2004
From: Ann Marie Stone
NRC/RGN-III/DRP/RPB3
To: Crane C
Exelon Generation Co, Exelon Nuclear
References
IR-04-007
Download: ML043060332 (36)


Text

October 29, 2004

SUBJECT:

BRAIDWOOD STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000456/2004007; 05000457/2004007

Dear Mr. Crane:

On September 30, 2004, the U. S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your Braidwood Station, Units 1 and 2. The enclosed report documents the inspection findings which were discussed on September 30, 2004, with Mr. T. Joyce and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, one NRC-identified finding of very low safety significance, which involved a violation of NRC requirements, was identified. However, because the violation was of very low safety significance and because the issue was entered into the licensees corrective action program, the NRC is treating the finding as a Non-Cited Violation in accordance with Section VI.A.1 of the NRCs Enforcement Policy. Additionally, a licensee-identified violation is listed in Section 4OA7 of this report.

If you contest the subject or severity of a Non-Cited Violation, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -

Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident Inspector Office at the Braidwood facility. In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Ann Marie Stone, Chief Branch 3 Division of Reactor Projects Docket Nos. 50-456; 50-457 License Nos. NPF-72; NPF-77

Enclosure:

Inspection Report 05000456/2004007; 05000457/2004007 w/Attachment: Supplemental Information

REGION III==

Docket Nos:

50-456; 50-457 License Nos:

NPF-72; NPF-77 Report No:

05000456/2004007; 05000457/2004007 Licensee:

Exelon Generation Company, LLC Facility:

Braidwood Station, Units 1 and 2 Location:

35100 S. Route 53 Suite 79 Braceville, IL 60407-9617 Dates:

July 1 through September 30, 2004 Inspectors:

S. Ray, Senior Resident Inspector N. Shah, Resident Inspector L. Haeg, Reactor Engineer J. House, Senior Radiation Specialist H. Peterson, Senior Operations Engineer R. Skokowski, Senior Resident Inspector, Byron Station P. Snyder, Resident Inspector, Byron Station T. Tongue, Project Engineer P. Smith, Illinois Emergency Management Agency Observers:

S. Cameron, Student Engineer J. Robbins, Reactor Engineer A. Wichman, Student Engineer M. Wilke, Reactor Engineer Approved by:

Ann Marie Stone, Chief Branch 3 Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000456/2004007, 05000457/2004007; 07/01/04 - 09/30/04; Braidwood Station,

Units 1 & 2; Post-Maintenance and Surveillance Testing.

This report covers a 3-month period of baseline resident inspection and an announced baseline inspection on radiation protection. The inspection was conducted by Region III inspectors and the resident inspectors. One Green finding associated with a Non-Cited Violation was identified. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 3, dated July 2000.

A.

Inspector-Identified and Self-Revealed Findings

Cornerstone: Barrier Integrity

Green.

The inspectors identified a finding of very low safety significance when they noted that the procedures for operating the hydrogen recombiners, if followed as written, would have resulted in the recombiners operating at too low of a temperature to be effective. This was due to a revision that changed the startup procedure, but not the panel lineup and shutdown procedures. The causes of this violation were related to the cross-cutting areas of Human Performance, because a system engineer failed to properly revise the procedures, and Problem Identification and Resolution, because the purpose of the revision was as a corrective action for a previously identified violation and was not effective. The condition existed for a period of 2 weeks before being identified and corrected through another procedure revision.

The finding was more than minor because it affected the Barrier Integrity cornerstone objective of providing reasonable assurance that the physical containment barrier would protect the public from radio nuclide releases caused by accidents or events. The finding was of very low safety significance because the hydrogen recombiner system is not a significant contributor to the large early release frequency for pressurized water reactors with large dry containments. This issue was determined to be a non-cited violation of 10 CFR 50, Appendix B, Criteria V, for procedures that were not appropriate to the circumstances. (Section 1RST)

Licensee-Identified Violations

A violation of very low safety significance, which was identified by the licensee as been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. This violation and the licensees corrective action tracking number is listed in Section 4OA7 of this report.

REPORT DETAILS

Summary of Plant Status

Unit 1 operated at or near full power for the entire inspection period except that power was reduced to about 88 percent from July 4 through July 6, 2004, for turbine and governor valve testing. On about September 27 the licensee began a gradual coastdown of power in preparation for a refueling outage. Power had been reduced to about 95 percent at the end of the inspection period.

Unit 2 operated at or near full power for the entire inspection period except that power was reduced to 86 percent on September 27 for turbine and governor valve testing.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment

.1 Complete Walkdowns

a. Inspection Scope

The inspectors performed a complete system walkdown of the Unit 2 safety injection system. This walkdown represented one inspection sample. This system was selected because it emergency core cooling system (ECCS) valves were a moderately high contributor to the overall core damage frequency in the licensees probabilistic risk analysis.

In addition to the walkdown, the inspectors reviewed the following:

  • selected operating, emergency, and surveillance procedures which involved manipulations of safety injection valves;
  • condition reports (CRs) for the system initiated within the last year; and
  • outstanding system work orders (WOs).

The inspectors also reviewed the CRs to determine whether issues were being properly addressed in the licensees corrective actions program. Documents reviewed as part of this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

.2 Partial Walkdowns

a. Inspection Scope

The inspectors performed partial walkdowns of the accessible portions of risk-significant system trains during periods when the train was of increased importance due to redundant trains or other equipment being unavailable. The inspectors utilized the valve and electric breaker checklists, as well as other documents listed in the Attachment, to determine that the components were properly positioned and that support systems were lined up as needed. The inspectors also examined the material condition of the components and observed operating parameters of equipment to confirm there were no obvious deficiencies. The inspectors reviewed outstanding WOs and CRs associated with the train to determine whether those documents revealed issues that could affect train function. The inspectors used the information in the appropriate sections of the TS and the UFSAR to determine the functional requirements of the system. The inspectors also reviewed the licensees identification of and the controls over the redundant risk-related equipment required to remain in service. The inspectors completed four samples of this requirement by walkdowns of the following trains:

  • the 1B centrifugal charging system prior to planned maintenance on the 1A chemical and volume control train;
  • the 1B essential service water pump during a planned work window on the 1A pump.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

Quarterly Area Walkdowns

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of fire fighting equipment, the control of transient combustibles and ignition sources, and on the condition and operating status of installed fire barriers. The inspectors selected fire areas for inspection based on their overall contribution to internal fire risk, as documented in the Individual Plant Examination of External Events with later additional insights or their potential to impact equipment which could initiate a plant transient. The inspectors used the documents listed in the to determine whether fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed; that transient material loading was within the analyzed limits; and that fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action program.

The inspectors completed ten samples of this inspection requirements during the following walkdowns:

  • main control room (Fire Zone 2.1-0);
  • division 12 engineered safety feature (ESF) switchgear room (Fire Zone 5.1-1);
  • division 11 ESF switchgear room (Fire Zone 5.2-1);
  • division 22 ESF switchgear room (Fire Zone 5.1-2);
  • division 21 ESF switchgear room (Fire Zone 5.2-2);
  • turbine building 451 foot elevation (Fire Zone 8.6-0);
  • turbine building 369 foot elevation Unit 1 (Fire Zones 8.1-0 and 8.2-1);
  • 1B DG room (Fire Zone 9.1-1); and
  • turbine building 369 foot elevation Unit 2 (Fire Zone 8.2-2).

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1 Quarterly Review of Testing/Training Activity

a. Inspection Scope

The inspectors observed an operating crew performance during an evaluated simulator out-of-the-box scenario. The inspectors evaluated crew performance in the following areas:

  • clarity and formality of communications;
  • ability to take timely actions in the safe direction;
  • prioritization, interpretation, and verification of alarms;
  • procedure use;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • group dynamics.

Crew performance in these areas was compared to licensee management expectations and guidelines as presented in the Exelon procedures listed in the Attachment.

The inspectors confirmed that the crew completed the critical tasks listed in the simulator guide. The inspectors also compared simulator configurations with actual control board configurations. For any weaknesses identified, the inspectors observed the licensee evaluators to determine whether they also noted the issues and discussed them in the critique at the end of the session. This inspection constituted one sample.

b. Findings

No findings of significance were identified.

.2 Biennial Written Examination and Annual Operating Test Results

a. Inspection Scope

The inspectors reviewed the overall pass/fail results of individual Job Performance Measure (JPM) operating tests, and simulator operating tests (required to be given per 10 CFR 55.59(a)(2)) administered by the licensee during calender year 2004. A written examination was conducted; however, it was not considered or taken credit for as the NRC comprehensive biennial examination. The overall results were compared with the significance determination process in accordance with NRC Manual Chapter 0609, Appendix I, Operator Requalification Human Performance Significance Determination Process (SDP).

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

Routine Inspection

a. Inspection Scope

The inspectors reviewed the licensees overall maintenance effectiveness for risk-significant event initiating, mitigating, and barrier integrity systems. This evaluation consisted of the following specific activities:

  • observing the conduct of planned and emergent maintenance activities where possible;
  • reviewing selected CRs, open WOs, and control room log entries in order to identify system deficiencies;
  • reviewing licensee system monitoring and trend reports;
  • attending various meetings throughout the inspection period where the status of maintenance rule activities was discussed;
  • a partial walkdown of the selected system; and
  • interviews with the appropriate system engineer.

The inspectors also reviewed whether the licensee properly implemented the Maintenance Rule, 10 CFR 50.65, for the system. Specifically, the inspectors determined whether:

  • performance problems constituted maintenance rule functional failures;
  • the system had been assigned the proper safety significance classification;
  • the system was properly classified as (a)(1) or (a)(2); and
  • the goals and corrective actions for the system were appropriate.

The above aspects were evaluated using the maintenance rule program and other documents listed in the Attachment. The inspectors also confirmed that the licensee was appropriately tracking reliability and/or unavailability for the systems.

The inspectors completed three samples in this inspection requirement by reviewing the following systems:

  • instrument power;

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensees management of plant risk during emergent maintenance activities or during activities where more than one significant system or train was unavailable. The activities were chosen based on their potential impact on increasing the probability of an initiating event or impacting the operation of safety-significant equipment. The inspections were conducted to determine whether evaluation, planning, control, and performance of the work were done in a manner to reduce the risk and minimize the duration where practical, and that contingency plans were in place where appropriate.

The licensees daily configuration risk assessments records, observations of operator turnover and plan-of-the-day meetings, observations of work in progress, and the documents listed in the Attachment were used by the inspectors to determine whether the equipment configurations were properly listed, that protected equipment were identified and were being controlled where appropriate, that work was being conducted properly, and that significant aspects of plant risk were being communicated to the necessary personnel. The inspectors confirmed that the licensee controlled emergent work in accordance with the expectations in the procedures listed in the Attachment.

In addition, the inspectors reviewed selected issues that the licensee entered into its corrective action program to determine whether identified problems were being entered into the program with the appropriate characterization and significance. The inspectors confirmed that minor issues identified during these inspections were entered into the licensee corrective action program.

The inspectors completed six samples by reviewing the following activities:

  • cleaning and testing of both trains of Unit 1 reactor containment fan coolers (RCFCs) following identification of low service water flow from fouling followed by thermal performance testing of the Unit 2 RCFCs;
  • operator response following an unplanned urgent failure of the Unit 1 rod control system;
  • operator response following an unplanned loss of the Unit 1 containment high-3 pressure sensing relay;
  • identification of low service water flow on the 2B RCFC during planned maintenance on the 2A DG and 2B component cooling (CC) pump;
  • an emergent issue with switchyard breaker 1-8 during planned maintenance on the 2B CC pump; and
  • planned maintenance on battery charger 211 requiring direct current (DC) cross-tie from Unit 2 DC bus 211 to Unit 1 DC bus 111.

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Non-Routine Evolutions and Events

a. Inspection Scope

The inspectors completed one sample by observing the following event:

  • an unplanned entry into 0BwOA Elec-1, Abnormal Grid Conditions-Unit 0, after the licensee was notified by the Transmissions Group of potential, degraded voltage conditions in the Units 1 and 2 switchyard.

For this event, the inspectors interviewed plant operators and reviewed plant records including control room logs, operator turnovers, and CRs. The inspectors confirmed that the control room response was consistent with 0BwOA Elec-1 and determined whether identified discrepancies were captured in the corrective action program.

Documents reviewed as part of this inspection are listed in the Attachment.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors evaluated plant conditions and selected CRs for risk-significant components and systems in which operability issues were questioned. These conditions were evaluated to determine whether the operability of components was justified. The inspectors compared the operability and design criteria in the appropriate section of the UFSAR to the licensees evaluations presented in the CRs and documents listed in the Attachment to determine whether the components or systems were operable. The inspectors also conducted interviews with the appropriate licensee system engineers and conducted plant walkdowns, as necessary, to obtain further information regarding operability questions. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action program.

The inspectors completed eight samples by reviewing the following operability evaluations and conditions:

  • Unit 1 rod control system following an unplanned rod control urgent failure alarm;
  • S hooks on electro-thermal links for fire dampers installed incorrectly;
  • Unit 1 and 2 lightning arrester system following several Unit 1 rod urgent failure alarms due to lightning strikes;
  • 2D RCFC flow instrument not responding;
  • failure of Instrument Inverter 114; and
  • discolored oil on the 2B CC pump outer bearing.

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

Annual Review

a. Inspection Scope

The inspectors evaluated the permanent plant modification installed under Engineering Change Request 348152 to relocate the sample lines for control room radiation monitors 0PR31J, 0PR32J and 0PR33J. This modification affected a safety-significant barrier integrity system and was one of the corrective actions in response to Licensee Event Report (LER) 2003-001-00, Control Room Ventilation System Alignment Results in Inoperable Radiation Monitors.

The inspectors reviewed the design change package and associated work orders for installation and observed the pre-job brief and actual installation of the modification.

After the modification was installed, the inspectors performed a walkdown of the radiation monitors to determine whether operation was proper. The inspectors confirmed that the modification did not introduce any new system vulnerabilities and did not create any new system interface problems. Documents reviewed as part of this inspection are listed in the Attachment. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action system.

This activity constituted one inspection sample of the annual requirement.

b. Findings

No findings of significance were identified.

1RST Post-Maintenance and Surveillance Testing - Pilot (71111.ST)

a. Inspection Scope

The inspectors reviewed post-maintenance and surveillance testing activities associated with important mitigating, barrier integrity, and support systems to ensure that the testing adequately demonstrated system operability and functional capability. For post-maintenance testing, the inspectors used the appropriate sections of the TS and UFSAR, as well as the WOs for the work performed, to evaluate the scope of the maintenance and to determine whether the post-maintenance testing was performed adequately, demonstrated that the maintenance was successful, and that operability was restored. For surveillance testing, the inspectors determined whether the testing met the TS, the UFSAR, and licensee procedural requirements, and demonstrated that the equipment was capable of performing its intended safety functions. The inspectors determined whether the testing met the frequency requirements; that the tests were conducted in accordance with the procedures, including establishing the proper plant conditions and prerequisites; that the test acceptance criteria was met; and that the results of the tests were properly reviewed and recorded. The activities were selected based on their importance in demonstrating mitigating systems capability and barrier integrity. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action program. Documents reviewed as part of this inspection are listed in the Attachment.

Note that this inspection is a pilot for a proposed consolidated procedure combining the previous Post-Maintenance Testing (71111.19) and Surveillance Testing (71111.22)procedures.

Five samples were completed by observing post-maintenance testing after the following activities:

  • planned maintenance of the 1A centrifugal charging pump;
  • planned maintenance on the 1B RH train;
  • planned maintenance on the 2A DG; and
  • emergent bearing change on the 2B CC pump.

Four samples were completed by observing and evaluating the following surveillance tests:

  • new fuel receipt and inspections; and
  • Unit 2 reactor containment fan coolers monthly surveillance testing.

b. Findings

Introduction:

The inspectors identified a Non-Cited Violation (NCV) of 10 CFR 50, Appendix B, Criteria V, having a very low safety significance (Green) for an inadequate procedure for startup of the hydrogen recombiners. The procedure, if followed as written, would have resulted in the recombiners operating at too low of a temperature to be effective.

Description:

As a result of one of the issues associated with a finding discussed in Inspection Report 05000456/2004004; 05000457/2004004, Section 1R15.1, the licensee revised the procedure for startup of the hydrogen recombiners (BwOP OG-10)on July 9, 2004. The revision removed the steps calling for manual adjustment of the reaction chamber gas temperature controller during startup to let the recombiner come up to the normal operating temperature of 1325 degrees Fahrenheit automatically as described in the UFSAR.

On July 23, 2004, the inspectors attended a pre-job briefing for a planned startup of the 0A hydrogen recombiner. The system engineer had proposed to demonstrate that the recombiner would operate properly with the revised procedure. During the briefing, an operator noted that the first step of the startup procedure required completion of the recombiner panel lineup sheet (BwOP OG-10T1). The panel lineup sheet called for the reaction chamber gas temperature controller to be set at 1100 degrees Fahrenheit and the operator questioned whether that was the correct value. The inspectors informed the operators that it appeared that the panel lineup sheet had not been revised when the startup procedure was revised. The inspectors also noted that the recombiner shutdown procedure (BwOP OG-9) also called for leaving the temperature controller set to 1100 degrees when the system was shutdown.

The work execution center supervisor called the system engineer who confirmed that both procedures should have been revised to list 1325 degrees, the normal recombiner operating temperature, instead of 1100 degrees. The system engineer stated that he had not realized that the panel lineup and shutdown procedures needed to be changed at the same time that the startup procedure was revised. The licensee revised both procedures to include the correct 1325 degree setpoint later on July 23, 2004, and the 0A recombiner was started up and operated.

Analysis:

The inspectors determined that failure to revise the panel lineup and shutdown procedures was a performance deficiency warranting a significance evaluation. Had a hydrogen recombiner been needed for an event between July 9 and July 23, 2004, and operators had followed the procedures as written, the recombiner reaction chamber gas temperature would have controlled at 1100 degrees rather than the 1325 degrees necessary for a proper oxygen/hydrogen recombination reaction. The same common procedure was used for both trains of recombiners so neither would have functioned properly in an event. The inspectors concluded that the finding was greater than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued on June 20, 2003. The inspectors answered yes to minor Question Number 4 because the finding was associated with the containment Barrier Integrity cornerstone attribute of risk important systems function and affected the cornerstone objective of providing reasonable assurance that the physical containment barrier would protect the public from radio nuclide releases caused by accidents or events. The function of the recombiners was to remove hydrogen from the containment, post accident, before it threatened containment integrity by reaching highly flammable concentrations. The finding also affected the cross-cutting areas of Human Performance, because the system engineer failed to revise two necessary procedures, and Problem Identification and Resolution, because the corrective action for the violation discussed in the previously mentioned inspection report was not adequately implemented.

The inspectors completed a significance determination of this issue using IMC 0609, Significance Determination Process, dated March 21, 2003. Using the Phase 1 screening worksheet in Appendix A, Attachment 1, dated September 10, 2004, the inspectors answered yes to Question 3 in the Containment Barriers column because the finding caused an actual reduction in defense-in-depth for the hydrogen control function of the reactor containment. The inspectors conducted a Phase 2 analysis using IMC 0609 Appendix H, Containment Integrity Significance Determination Process, dated May 6, 2004. The finding was screened as Green because it did not affect the core damage frequency and inoperability of the hydrogen recombiner did not have a significant effect on the large early release frequency for a pressurized water reactor with a large dry containment. In addition, the inspectors determined through discussions with operators and engineers, as well as observations of the emergency response organization, that the procedure discrepancies would probably have been identified and corrected in an actual event. Therefore, this finding was considered to be of very low safety significance (Green) and was assigned to the Barrier Integrity cornerstone of both units.

Enforcement:

Criterion V, Instructions, Procedures, and Drawings, of 10 CFR 50, Appendix B required, in part, that activities affecting quality shall be prescribed by documented instructions, procedures, or drawings, of a type appropriate to the circumstances and shall be accomplished in accordance with these instructions, procedures, or drawings. Contrary to the above, between July 9 and July 23, 2004, the procedures for operating the hydrogen recombiners were not appropriate because they would have resulted in the recombiners operating at too low a temperature to be effective. The procedures were revised on July 23, 2004, and demonstrated to be appropriate. The licensee entered the issue into its corrective action program as CR 238380. Because this violation was of very low safety significance and it was entered into the licensees corrective action program, this violation is being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy.

(NCV 05000456/2004007-01; 05000457/2004007-01)

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the current status of the Units 1 and 2 positive displacement pumps. These pumps were originally installed equipment that were not being used or maintained by the licensee, but which had not been officially classified as abandoned.

The positive displacement pumps were not considered safety-related, but did interface with the refueling water storage tank, a safety-related component, and were considered a backup pump to the safety-related centrifugal charging pumps. The inspectors determined that the change did not have an unanalyzed affect on the safety functions of important safety systems. As part of this inspection, the inspectors reviewed the 10 CFR 50.59 screening, appropriate UFSAR sections, and the TS, to determine whether system operability/availability was affected. The inspectors confirmed that minor issues identified during the inspection were entered into the licensees corrective action program. Documents reviewed as part of this inspection are listed in the

. This review constituted one sample of this inspection requirement.

b. Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed licensee performance during an evaluated emergency response drill. Observations included manning of the Technical Support Center (TSC),turnover of command and control to and from the TSC, event classification and notification, and development of protective action recommendations. The inspectors also observed Operations Support Center (OSC) activities and accompanied one in-plant team. The inspectors confirmed that deficiencies noted during the drill, by either the inspectors or licensee evaluators, were entered into the licensees corrective action program. The inspectors also attended portions of the post drill critique for the TSC and OSC crews. Documents reviewed as part of this inspection are listed in the Attachment.

This activity constituted one inspection sample.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Public Radiation Safety

2PS2 Radioactive Material Processing and Transportation (71122.02) Shipment Preparation

a. Inspection Scope

The inspectors reviewed shipment packaging and surveying, emergency instructions, disposal manifest, and shipping papers provided to the driver. The receiving licensees authorization to receive the shipment package was verified. Radiation worker practices were observed in order to verify that the workers had adequate skills to accomplish each task and to determine if the shippers were knowledgeable of the shipping regulations and whether shipping personnel demonstrated adequate skills to accomplish the package preparation requirements for public transport with respect to NRC Bulletin 79-19 and 49 CFR Part 172 Subpart H. The review was conducted to verify that the licensees training program provided training consistent with NRC and Department of Transportation requirements. These reviews represented one sample.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

Cornerstones: Mitigating Systems and Barrier Integrity

4OA1 Performance Indicator Verification

Reactor Safety Strategic Area

a. Inspection Scope

The inspectors reviewed the documents listed in the Attachment to determine whether the licensee had corrected reported performance indicator data, in accordance with the criteria in NEI [Nuclear Energy Institute] 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 2. The data reported by the licensee was compared to a sampling of control room logs, CRs, and other sources of data generated since the last verification. The inspectors determined that minor issues identified during the inspection were entered into the licensees corrective action program. The inspectors completed six samples by examining the following performance indicators:

Unit 1

  • safety system unavailability - auxiliary feedwater system for the period of July 1, 2003 through June 30, 2004;
  • safety system functional failures for the period of July 1, 2003 through June 30, 2004; and

Unit 2

  • safety system unavailability - auxiliary feedwater system for the period of July 1, 2003 through June 30, 2004;
  • safety system functional failures for the period of July 1, 2003 through June 30, 2004; and

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Identification and Resolution of Problems

a. Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to determine whether they were being entered into the licensees corrective action program at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Minor issues entered into the licensees corrective action program as a result of the inspectors observations are generally denoted in the Attachment. These activities were part of normal inspection activities and were not considered separate samples.

b. Findings

No finding of significance were identified.

.2 Boric Acid Leakage Identification and Resolution (Annual Sample)

Introduction The inspectors reviewed the licensees process for identifying and resolving borated water leaks. The inspection focused on how identified leakage was being identified, how it was documented and tracked, and what corrective actions were taken. The inspectors were particularly concerned with how the licensee addressed those components particularly susceptible to boric acid corrosion. This inspection was prompted by an apparent increasing trend in the number of borated water leaks the licensee had identified over the past year. Additionally, this inspection was also planned to review the effectiveness of the licensees new boric acid control program, which was implemented in August 2003. As a guide in this program, the inspectors referred to the Electric Power and Research Institute document No. 1000975, Boric Acid Corrosion Guidebook, Revision 1.

a.

Effectiveness of Problem Identification

(1) Inspection Scope The inspectors reviewed those station procedures implementing the licensees boric acid control program. The inspectors also reviewed the CRs listed in the Attachment to determine whether borated water leaks were being properly identified and evaluated.

The inspectors performed walkdowns of selected areas of the auxiliary building to observe boric acid leakage and conducted interviews with selected licensee staff to determine whether the boric acid program requirements were understood.

(2) Issues The licensees procedures required that boric acid leakage be documented in CRs and routed to the station Boric Acid Control Coordinator (BACC) for review. The BACC was responsible for tracking, evaluating and resolving boric acid leaks. The inspectors noted that the procedures were consistent with the aforementioned industry document including identifying specific components and systems susceptible to boric acid corrosion.

During interviews, the BACC stated that the increase in CRs resulted from a renewed emphasis on identifying and resolving boric acid leakage following the implementation of the new program and in light of recent industry lessons learned. This resulted in more frequent plant walkdowns by the BACC and an increased awareness among plant staff following supplemental training on the new program requirements.

The inspectors observed that the majority of the boric acid CRs generated over the past year were written by the BACC. There were some CRs generated by the other work groups, primarily radiation protection and operations staff, however, the BACC stated that most boric acid issues were verbally communicated to him. The BACC maintained a database of all identified leaks tracking, in part, the date of identification, current status and planned corrective actions.

During plant walkdowns, the inspectors noted that most observed leaks were recorded in the BACC database. Those leaks identified by the inspectors, but not in the database, were documented in CRs by the BACC. The inspectors also noted that, when interviewed, licensee staff generally understood the boric acid program requirements.

However, the inspectors identified some instances where leaks from borated water systems were documented in CRs, but were not sent to the BACC for review. The specific examples did not affect the operability of safety-significant systems, but did indicate a possible lack of sensitivity to boric acid leakage during the licensees CR review process. The BACC documented this issue in a CR for followup.

b.

Effectiveness of Corrective Actions

(1) Inspection Scope The inspectors reviewed CRs documenting boric acid leakage and the BACC database to determine whether the licensee was effectively addressing boric acid leakage concerns. Specifically, for selected issues, the inspectors reviewed the as found reports, the associated engineering evaluation, the proposed corrective actions and interviewed licensee personnel. As part of this review, the inspectors performed plant walkdowns to observe the condition of the repaired components.
(2) Issues The licensee appeared to be properly evaluating and correcting boric acid leaks.

Specifically, the inspectors noted that the evaluations identified the source and nature of the deposits, the operability of the affected components, whether the leakage was recurring, the planned corrective actions and, if the issue had been resolved, whether the corrective actions were effective. There was also reasonable and sufficient documentation for each issue.

The corrective actions for the reviewed items appeared adequate, were focused on the apparent cause for each condition and were appropriately scheduled for timeliness. The inspectors observed that active leaks having interim corrective actions, but not yet repaired, were contained and that there was no apparent further component degradation. For those leaks considered permanently repaired, the inspectors observed no recurrence of leakage.

4OA3 Event Followup

The inspectors completed four inspection samples in this area.

.1 Licensee Event Report Review

a.

(Closed) LER 05000456/2004-002-00: 1C Reactor Containment Fan Cooler Discovered to be Inoperable Greater Than Required TS Allowed Outage Time On June 1, 2004, during a monthly surveillance test, the licensee discovered that the essential service water flow rate through the 1C RCFC was below the limit of 2660 gallons per minute (gpm) of TS 3.6.6. The licensees investigation determined that the flow had been below the TS limit since May 6, 2004, a period longer than the 7-day allowed outage time of the TS. The flow had been set too low in May due to the fact that the flow indication was inaccurate due to partial blocking from calcium carbonate deposits. Corrective actions, as discussed in the LER and in CR 224989, included cleaning and calibrating the flow detectors of all the RCFCs, resetting the flow control throttling valve for the 1C RCFC, and strengthening the program for creating and implementing adverse condition monitoring plans.

The inspectors concluded that the issue was greater than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition Screening, issued on June 20, 2003. The inspectors answered yes to minor Question Number 4 because the finding was associated with the containment Barrier Integrity cornerstone attribute of risk important systems function and affected the cornerstone objective of providing reasonable assurance that the physical containment barrier would protect the public from radio nuclide releases caused by accidents or events. The function of the RCFCs was to remove heat to limit the post-accident pressure in the containment.

The inspectors completed a significance determination of this issue using IMC 0609, Significance Determination Process, dated March 21, 2003. Using the Phase 1 screening worksheet in Appendix A, Attachment A, dated September 10, 2004, the inspectors answered yes to Question 3 in the Containment Barriers column because the finding caused an actual reduction in defense-in-depth for the atmospheric pressure control function of the reactor containment. The inspectors conducted a Phase 2 analysis using IMC 0609 Appendix H, Containment Integrity Significance Determination Process, dated May 6, 2004. The finding was screened as Green because it did not affect the core damage frequency and inoperability of an RCFC did not have a significant effect on the large early release frequency for a pressurized water reactor with a large dry containment. In addition, as discussed in the LER, based on the actual essential service water temperature during the period of inoperability, there was only a short period of time where even the degraded train of RCFCs alone would not have been able to perform its safety function. Therefore, this finding was considered to be of very low safety significance (Green) and was assigned to the Barrier Integrity cornerstone of Unit 1.

This licensee-identified finding involved a violation of TS 3.6.6, Containment Spray and Cooling Systems. The enforcement aspects of the violation are discussed in Section 4OA7. This LER is closed.

b.

(Closed) LER 05000456/2004-003-00: 0A Hydrogen Recombiner Identified to be Inoperable Greater Than the Required TS Allowed Outage Time On June 16, 2004, the licensee identified that the 0A hydrogen recombiner had been inoperable in excess of the 30 day Allowed Outage Time permitted by TS 3.6.8.

Specifically, the recombiner had been inoperable since March 3, 2004, when the heater breaker tripped during post-maintenance testing. This issue was previously considered a Non-Cited Violation and a finding of very low safety significance (Green). This issue was assigned to the Barrier Integrity cornerstone of both units since the 0A recombiner could serve either unit. The specifics of the issue including the inspectors review and significance determination were discussed in NRC Inspection Report 05000456/2004004; 05000457/2004004. This LER is closed.

.2 Notification of Loss of Emergency Preparedness Capabilities

On August 4, 2004, the licensee notified the NRC via the Emergency Notification System, that it had experienced a major loss of emergency preparedness capabilities.

Due to lightening and severe weather the night of August 3-4, 2004, the licensee experienced short periods where more than 25 percent of their offsite notification sirens were inoperable. The longest period was for about 42 minutes. The inspectors reviewed the records and determined that the public notification capabilities were restored in a timely manner and that the problem had been entered into the licensees corrective action program. This issue was not a violation of NRC requirements.

.3 Increase in Unit 1 Containment Noble Gas Levels

a. Inspection Scope

On August 5, 2004, the licensee recognized an increase in Unit 1 containment noble gas levels, which indicated a small reactor coolant system leak. The leak was so small that there was no discernable increase in the leak rate calculation performed. On August 9, 2004, licensee personnel completed a containment tour and identified a small steam leak at a fitting on the pressurizer steam space sample line. Although the sample line was isolated, it appeared that the isolation valve (1PS9350A) was leaking by. The licensee evaluated the leak rate and the impact of the leak with no significant concerns identified. On August 12, 2004, the licensee performed another containment entry and closed a manual isolation upstream of the leak and effectively stopped the leak.

From the time the licensee identified the increase in noble gases, until the licensee stopped the leak on August 12, 2004, the inspectors monitored the leak rate, and the licensees performance to address the concern. This included accompanying licensee personnel during the containment entry on August 12, 2004. The inspectors confirmed that the leak rate levels never approached the TS limits. Also, the inspectors assess the leak-by associated with the isolation valve 1PS9350A and confirmed that the condition was not prohibited by TS. Documents reviewed as part of this inspection were listed in the Attachment.

b. Findings

No findings of significance were identified.

.4 Notification of a Minor Oil Spill

On September 13, 2004, the licensee notified the NRC via the Emergency Notification System that it had notified the appropriate agencies of a small hydraulic oil spill on the property adjacent to the station. The inspectors determined that the event was not a significant NRC regulatory concern and did no followup. This activity was not considered an inspection sample but was included in the report to complete the public record.

4OA4 Cross-Cutting Aspects of Findings

.1 The finding described in Section 1RST of this report had, as one of its causes, a human

performance deficiency, in that, the system engineer failed to revise two other applicable procedures when revising the startup procedure for the hydrogen recombiners, resulting in procedures that would not have worked if called upon.

.2 The finding described in Section 1RST of this report also had, as another one of its

causes, a problem identification and resolution deficiency, in that, the licensee corrective actions following a previously identified violation for the hydrogen recombiners were not effective.

4OA5 Other Activities

Review of Institute of Nuclear Power Operations Report The inspectors completed a review of the final report for the Institute of Nuclear Power Operations, January 2004 Evaluation, dated July 23, 2004.

4OA6 Meetings

Exit Meeting The inspectors presented the inspection results to Mr. T. Joyce and other members of licensee management at the conclusion of the inspection on September 30, 2004. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance were identified by the licensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Manual, NUREG-1600, for being dispositioned as NCVs.

Cornerstone: Barrier Integrity

Technical Specification 3.6.6 required that two containment spray trains and two containment cooling trains shall be operable in Modes 1, 2, 3, and 4. With one or more containment cooling trains inoperable the trains must be restored to operable within 7 days or the unit be placed in Mode 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. Surveillance Requirement 3.6.6.3 for demonstrating operability of the containment cooling train required that cooling water flow rate be greater than or equal to 2660 gpm. As described in LER 05000456/2004-002-00 and Section 4OA3.1a of this report, between May 6, 2004, and June 1, 2004, the cooling water flow to the 1C RCFC was less than 2660 gpm. The licensee entered this issue into its corrective action program as CR 224989.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

T. Joyce, Site Vice President
K. Polson, Plant Manager
D. Ambler, Regulatory Assurance Manager
D. Burton, Licensed Operator Requalification Training Group Lead
S. Butler, Regulatory Assurance - NRC Coordinator
G. Dudek, Operations Director
R. Gilbert, Nuclear Oversight Manager
J. Kuczynski, Chemistry Manager
D. Morse, Radioactive Materials Shipper
J. Moser, Radiation Protection Manager
M. Smith, Engineering Director
E. Wrigley, Maintenance Director

Nuclear Regulatory Commission

A. Stone, Chief, Reactor Projects Branch 3

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened

05000456/2004007-01;
05000457/2004007-01 NCV Failure to Have Appropriate Procedures for Operation of the Hydrogen Recombiners (Section 1RST)

Closed

05000456/2004007-01;
05000457/2004007-01 NCV Failure to Have Appropriate Procedures for Operation of the Hydrogen Recombiners (Section 1RST)
05000456/2004-002-00 LER 1C Reactor Containment Fan Cooler Discovered to be Inoperable Greater Than Required TS Allowed Outage Time (Section 4OA3.1a)
05000456/2004-003-00 LER 0A Hydrogen Recombiner Identified to be Inoperable Greater Than the Required TS Allowed Outage Time (Section 4OA3.1b)

Discussed

None.

LIST OF DOCUMENTS REVIEWED