IR 05000331/2005011: Difference between revisions
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{{#Wiki_filter: | {{#Wiki_filter:July 1, 2005 | ||
==SUBJECT:== | ==SUBJECT:== | ||
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The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license. | The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license. | ||
The purpose of this inspection was to assess the safety significance and any necessary regulatory actions associated with the primary system hydrostatic test, VT- 2 inspections, and control rod testing activities that occurred at Duane Arnold on April 26 and 27, 2005. Within these areas, the inspection consisted of interviews with personnel and the selected examination of procedures and representative records. | The purpose of this inspection was to assess the safety significance and any necessary regulatory actions associated with the primary system hydrostatic test, VT-2 inspections, and control rod testing activities that occurred at Duane Arnold on April 26 and 27, 2005. Within these areas, the inspection consisted of interviews with personnel and the selected examination of procedures and representative records. | ||
Based upon the results of this inspection, the NRC identified two issues that were evaluated under the risk significance determination process as having very low safety significance (green). | Based upon the results of this inspection, the NRC identified two issues that were evaluated under the risk significance determination process as having very low safety significance (green). | ||
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The NRC determined that violations were associated with each of the two issues. One of the issues was also evaluated in accordance with the NRC Enforcement Policy and was determined to be a Severity Level IV violation of NRC requirements. The current Enforcement Policy is included on the NRCs Web site as www.nrc.gov; select What We Do, Enforcement and Enforcement Policy. The violations are cited in the enclosed Notice of Violation (Notice) and the circumstances surrounding the violations are described in detail in the subject inspection report. The violations are being cited in the enclosed Notice because you failed to restore compliance within a reasonable time period after the violations were identified and you failed to enter the issues into your corrective action program to address recurrence. The violations involved your failure to comply with the requirements of Technical Specification 3.10.1, System Leakage and Hydrostatic Testing, and 10 CFR 50.59, Changes, Tests, and Experiments. | The NRC determined that violations were associated with each of the two issues. One of the issues was also evaluated in accordance with the NRC Enforcement Policy and was determined to be a Severity Level IV violation of NRC requirements. The current Enforcement Policy is included on the NRCs Web site as www.nrc.gov; select What We Do, Enforcement and Enforcement Policy. The violations are cited in the enclosed Notice of Violation (Notice) and the circumstances surrounding the violations are described in detail in the subject inspection report. The violations are being cited in the enclosed Notice because you failed to restore compliance within a reasonable time period after the violations were identified and you failed to enter the issues into your corrective action program to address recurrence. The violations involved your failure to comply with the requirements of Technical Specification 3.10.1, System Leakage and Hydrostatic Testing, and 10 CFR 50.59, Changes, Tests, and Experiments. | ||
You are required to respond to this letter and should follow the instructions specified in the enclosed Notice when preparing your response. The NRC will use your response, in part, to determine whether further enforcement action is necessary to ensure compliance with G. Van Middlesworth | You are required to respond to this letter and should follow the instructions specified in the enclosed Notice when preparing your response. The NRC will use your response, in part, to determine whether further enforcement action is necessary to ensure compliance with G. Van Middlesworth-2- | ||
regulatory requirements. During the discussion of the violations at the exit, your staff indicated that they did not agree with the violations, and would include the basis for the disagreement in the response to our Notice of Violation. | regulatory requirements. During the discussion of the violations at the exit, your staff indicated that they did not agree with the violations, and would include the basis for the disagreement in the response to our Notice of Violation. | ||
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REGION III== | REGION III== | ||
Docket No: 50-331 License No: DPR-49 Report No: 05000331/2005011 Licensee: Nuclear Management Company, LLC Facility: Duane Arnold Energy Center Location: 3277 DAEC Road Palo, Iowa 52324-9785 Dates: April 25, 2005 through June 03, 2005 Inspectors: G. Wilson, Senior Resident Inspector R. Baker, Resident Inspector Approved by: Bruce L. Burgess, Chief Branch 2 Division of Reactor Projects Enclosure | Docket No: | ||
50-331 License No: | |||
DPR-49 Report No: | |||
05000331/2005011 Licensee: | |||
Nuclear Management Company, LLC Facility: | |||
Duane Arnold Energy Center Location: | |||
3277 DAEC Road Palo, Iowa 52324-9785 Dates: | |||
April 25, 2005 through June 03, 2005 Inspectors: | |||
G. Wilson, Senior Resident Inspector R. Baker, Resident Inspector Approved by: | |||
Bruce L. Burgess, Chief Branch 2 Division of Reactor Projects | |||
Enclosure | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
| Line 60: | Line 71: | ||
Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000. | Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000. | ||
A. | A. | ||
Inspector-Identified and Self-Revealed Findings | |||
===Cornerstone: Mitigating Systems=== | ===Cornerstone: Mitigating Systems=== | ||
* | |||
: '''Green.''' | : '''Green.''' | ||
The inspectors identified that the licensee was not in compliance with Technical Specification 3.10.1, System Leakage and Hydrostatic Testing Operation. The non-compliance occurred when the licensee remained above 212°F to performed SCRAM time testing after completion of the reactor coolant system hydrostatic testing and required VT- 2 leakage inspections on April 26 and 27, 2005. Therefore, the operating exemptions allowed by TS 3.10.1 for the system leakage tests would not be applicable. | The inspectors identified that the licensee was not in compliance with Technical Specification 3.10.1, System Leakage and Hydrostatic Testing Operation. The non-compliance occurred when the licensee remained above 212°F to performed SCRAM time testing after completion of the reactor coolant system hydrostatic testing and required VT-2 leakage inspections on April 26 and 27, 2005. Therefore, the operating exemptions allowed by TS 3.10.1 for the system leakage tests would not be applicable. | ||
Because the issue was not entered into your corrective action program and you did not restore compliance within a reasonable period of time, a Notice of Violation is being issued. The finding was determined to be of very low safety significance since the procedure was performed at the end of an outage, when the decay heat rate was very low, and multiple trains of emergency core cooling systems were available for accident purposes. This was determined to be a TS 3.10.1 violation associated with a Green finding. (Section 1R20) | Because the issue was not entered into your corrective action program and you did not restore compliance within a reasonable period of time, a Notice of Violation is being issued. The finding was determined to be of very low safety significance since the procedure was performed at the end of an outage, when the decay heat rate was very low, and multiple trains of emergency core cooling systems were available for accident purposes. This was determined to be a TS 3.10.1 violation associated with a Green finding. (Section 1R20) | ||
* | |||
: '''Green.''' | : '''Green.''' | ||
The inspectors identified that a change to the procedures for the Non-Nuclear Heat Class 1 System Leakage Pressure Tests required prior NRC approval. The procedural changes lengthened the amount of time that the reactor coolant system would exceed 212°F, an unplanned mode change, and added control rod drive scram time testing. These procedural changes resulted in a need for a change in the Technical Specifications (TS) 3.10.1, System Leakage and Hydrostatic Testing Operation. | The inspectors identified that a change to the procedures for the Non-Nuclear Heat Class 1 System Leakage Pressure Tests required prior NRC approval. The procedural changes lengthened the amount of time that the reactor coolant system would exceed 212°F, an unplanned mode change, and added control rod drive scram time testing. These procedural changes resulted in a need for a change in the Technical Specifications (TS) 3.10.1, System Leakage and Hydrostatic Testing Operation. | ||
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===Licensee-Identified Violations=== | ===Licensee-Identified Violations=== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
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==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity=== | ===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity=== | ||
{{a|1R20}} | {{a|1R20}} | ||
==1R20 Outage Activities== | ==1R20 Outage Activities== | ||
{{IP sample|IP=IP 71111.20}} | {{IP sample|IP=IP 71111.20}} | ||
===.1 Refueling Outage=== | ===.1 Refueling Outage=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors observed outage activities for Scheduled Refueling Outage Number 19 during this inspection period. Outage configuration management was monitored by verifying that the licensee maintained appropriate defense in depth to address all shutdown safety functions and satisfy Technical Specification (TS) requirements. The documents listed in the Attachment were used to accomplish the objectives of the inspection procedure. This inspection will not count as an annual sample. | The inspectors observed outage activities for Scheduled Refueling Outage Number 19 during this inspection period. Outage configuration management was monitored by verifying that the licensee maintained appropriate defense in depth to address all shutdown safety functions and satisfy Technical Specification (TS) requirements. The documents listed in the Attachment were used to accomplish the objectives of the inspection procedure. This inspection will not count as an annual sample. | ||
====b. Findings==== | ====b. Findings==== | ||
===1. Technical Specification 3.10.1 Compliance=== | ===1. Technical Specification 3.10.1 Compliance=== | ||
=====Introduction:===== | =====Introduction:===== | ||
The inspectors identified that the licensee failed to comply with TS 3.10.1 System Leakage and Hydrostatic Testing Operation, requirements. The issue was considered to be of very low safety significance (Green). | The inspectors identified that the licensee failed to comply with TS 3.10.1 System Leakage and Hydrostatic Testing Operation, requirements. The issue was considered to be of very low safety significance (Green). | ||
=====Description:===== | =====Description:===== | ||
On April 26, 2005, the inspectors identified that the licensee was not in compliance with Special Operations TS 3.10.1, System Leakage and Hydrostatic Testing Operation. The non-compliance was due to the failure to cool down the plant following completion of the reactor coolant system hydro and VT- 2 inspections. The licensee extended the operation of the plant with temperatures greater than 212°F to perform SCRAM time testing, which was completed on April 27, 2005. The inspectors questioned the licensees compliance with TS 3.10.1, since the operating exemptions for plant operation only apply for system leakage and hydrostatic testing, therefore the exemptions are not applicable for SCRAM time testing. Because SCRAM time testing was performed after the leakage inspections were complete, the operating exemptions allowed by TS 3.10.1 for system leakage tests would not be applicable. During the extension of the time that the plant was greater than 212°F for SCRAM time testing, the plant would be considered to be in Mode 3 without having all the requirements necessary for Mode 3 operation. The inspectors first questioned the licensees TS compliance on April 26, 2005 during a discussion with the Operations Shift Manager. | On April 26, 2005, the inspectors identified that the licensee was not in compliance with Special Operations TS 3.10.1, System Leakage and Hydrostatic Testing Operation. The non-compliance was due to the failure to cool down the plant following completion of the reactor coolant system hydro and VT-2 inspections. The licensee extended the operation of the plant with temperatures greater than 212°F to perform SCRAM time testing, which was completed on April 27, 2005. The inspectors questioned the licensees compliance with TS 3.10.1, since the operating exemptions for plant operation only apply for system leakage and hydrostatic testing, therefore the exemptions are not applicable for SCRAM time testing. Because SCRAM time testing was performed after the leakage inspections were complete, the operating exemptions allowed by TS 3.10.1 for system leakage tests would not be applicable. During the extension of the time that the plant was greater than 212°F for SCRAM time testing, the plant would be considered to be in Mode 3 without having all the requirements necessary for Mode 3 operation. The inspectors first questioned the licensees TS compliance on April 26, 2005 during a discussion with the Operations Shift Manager. | ||
Additional discussions with the licensee occurred on April 27, 2005, and involved the Site Director, Plant Manager, and the Regulatory Affairs Manager. Even though the inspectors challenged the compliance with TS 3.10.1, the licensee continued to perform SCRAM time testing until it was completed and then commenced a plant cool down. No actions were performed to resolve the non-compliance. Upon further evaluation, the inspectors identified that the licensee had also violated the requirements of TS 3.10.1 to perform SCRAM time testing during the Class 1 System Leakage Pressure Test for the following periods: November 23, 1999, through November 25, 1999, May 18, 2001, through May 21, 2001, and April 15, 2003, through April 16, 2003. | Additional discussions with the licensee occurred on April 27, 2005, and involved the Site Director, Plant Manager, and the Regulatory Affairs Manager. Even though the inspectors challenged the compliance with TS 3.10.1, the licensee continued to perform SCRAM time testing until it was completed and then commenced a plant cool down. No actions were performed to resolve the non-compliance. Upon further evaluation, the inspectors identified that the licensee had also violated the requirements of TS 3.10.1 to perform SCRAM time testing during the Class 1 System Leakage Pressure Test for the following periods: November 23, 1999, through November 25, 1999, May 18, 2001, through May 21, 2001, and April 15, 2003, through April 16, 2003. | ||
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=====Enforcement:===== | =====Enforcement:===== | ||
Special Operations TS 3.10.1, System Leakage and Hydrostatic Testing, allows exemptions of reactor coolant temperature requirements for the performance of system leakage and hydrostatic testing. The exemptions allows the plant to go above 212°F and still be considered in Mode 4 even though the associated temperature would be Mode 3 for system leakage tests. Contrary to this requirement, the licensee extended the plant operation time with reactor coolant temperature greater than 212°F from April 26 through April 27, 2005, to perform SCRAM time testing following the completion of the VT- 2 inspections for the systems leakage test. Furthermore, the licensee failed to restore compliance within a reasonable period of time after the issue was identified to your staff on April 26, 2005. In addition, the licensee also failed to comply with the requirements of TS 3.10.1 during the following periods: November 23, 1999, through November 25,1999, May 18, 2001, through May 21, 2001, and April 15, 2003, through April 16, 2003. The failure to comply with the requirements of TS 3.10.1 was a violation. | Special Operations TS 3.10.1, System Leakage and Hydrostatic Testing, allows exemptions of reactor coolant temperature requirements for the performance of system leakage and hydrostatic testing. The exemptions allows the plant to go above 212°F and still be considered in Mode 4 even though the associated temperature would be Mode 3 for system leakage tests. Contrary to this requirement, the licensee extended the plant operation time with reactor coolant temperature greater than 212°F from April 26 through April 27, 2005, to perform SCRAM time testing following the completion of the VT-2 inspections for the systems leakage test. Furthermore, the licensee failed to restore compliance within a reasonable period of time after the issue was identified to your staff on April 26, 2005. In addition, the licensee also failed to comply with the requirements of TS 3.10.1 during the following periods: November 23, 1999, through November 25,1999, May 18, 2001, through May 21, 2001, and April 15, 2003, through April 16, 2003. The failure to comply with the requirements of TS 3.10.1 was a violation. | ||
Since the licensee failed to restore compliance within a reasonable time after the violation was identified and they did not place the violation into a corrective action program to prevent recurrence, a Notice of Violation (NOV) is being issued for this violation associated with a Green finding, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NOV 05000331/2005011-01) | Since the licensee failed to restore compliance within a reasonable time after the violation was identified and they did not place the violation into a corrective action program to prevent recurrence, a Notice of Violation (NOV) is being issued for this violation associated with a Green finding, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NOV 05000331/2005011-01) | ||
Procedures Changes for Non-Nuclear Heat Class 1 System Leakage Pressure Tests | |||
=====Introduction:===== | =====Introduction:===== | ||
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10 CFR 50.59, Changes, tests, and experiments, states, in part, the holder of a license authorizing operation of a production or utilization facility may conduct tests not described in the safety analysis report, without prior Commission approval, unless the proposed test involves a change in the technical specifications incorporated in the license. Contrary to this, on August 19, 1999, the licensee implemented a change to STP 3.10.1.01 and STP 3.10.1-02 which resulted in the need for a change in the TS. The result of the violation was determined to be of very low safety significance; therefore, this violation of 10 CFR 50.59 was classified as a Severity Level IV violation. Since the licensee failed to restore compliance within a reasonable time after the violation was identified and they did not place the violation into a corrective action program to prevent recurrence, a Notice of Violation (NOV) is being issued for this Severity Level IV violation, consistent with Section VI.A.1 of the NRC Enforcement Policy. | 10 CFR 50.59, Changes, tests, and experiments, states, in part, the holder of a license authorizing operation of a production or utilization facility may conduct tests not described in the safety analysis report, without prior Commission approval, unless the proposed test involves a change in the technical specifications incorporated in the license. Contrary to this, on August 19, 1999, the licensee implemented a change to STP 3.10.1.01 and STP 3.10.1-02 which resulted in the need for a change in the TS. The result of the violation was determined to be of very low safety significance; therefore, this violation of 10 CFR 50.59 was classified as a Severity Level IV violation. Since the licensee failed to restore compliance within a reasonable time after the violation was identified and they did not place the violation into a corrective action program to prevent recurrence, a Notice of Violation (NOV) is being issued for this Severity Level IV violation, consistent with Section VI.A.1 of the NRC Enforcement Policy. | ||
(NOV 05000331/2005011-02) | |||
{{a|4OA6}} | {{a|4OA6}} | ||
==4OA6 Meetings== | ==4OA6 Meetings== | ||
===1. Exit Meeting=== | ===1. Exit Meeting=== | ||
The inspectors presented the inspection results to Mr. J. Bjorseth and other members of licensee management on June 03, 2005. During the discussion of the violations at the exit, your staff indicated that they did not agree with the violations, and would include the basis for the disagreement in the response to our Notice of Violation. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified. | The inspectors presented the inspection results to Mr. J. Bjorseth and other members of licensee management on June 03, 2005. During the discussion of the violations at the exit, your staff indicated that they did not agree with the violations, and would include the basis for the disagreement in the response to our Notice of Violation. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified. | ||
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==KEY POINTS OF CONTACT== | ==KEY POINTS OF CONTACT== | ||
Licensee | Licensee | ||
: [[contact::G. Van Middlesworth]], Site Vice President | : [[contact::G. Van Middlesworth]], Site Vice President | ||
| Line 163: | Line 173: | ||
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED== | ==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED== | ||
===Opened=== | ===Opened=== | ||
: 05000331/2005011-01 | : 05000331/2005011-01 NOV Failure to Comply with the Requirements of TS 3.10.1 during the Performance of the Non-Nuclear Heat Class 1 System Leakage Pressure Test | ||
: 05000331/2005011-02 | : 05000331/2005011-02 NOV Failure to Comply with the Requirements of 10 CFR 50.59 for a Change to the Procedures for Non-Nuclear Heat Class System Leakage Pressure Tests | ||
===Closed=== | ===Closed=== | ||
None. | None. | ||
===Discussed=== | ===Discussed=== | ||
None. | None. | ||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} | ||
Latest revision as of 17:52, 15 January 2025
| ML051860395 | |
| Person / Time | |
|---|---|
| Site: | Duane Arnold |
| Issue date: | 07/01/2005 |
| From: | Satorius M NRC/RGN-III |
| To: | Vanmiddlesworth G Nuclear Management Co |
| References | |
| IR-05-011 | |
| Download: ML051860395 (16) | |
Text
July 1, 2005
SUBJECT:
DUANE ARNOLD ENERGY CENTER NRC INSPECTION REPORT 5000331/2005011 AND NOTICE OF VIOLATION
Dear Mr. Van Middlesworth:
On June 3, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at the Duane Arnold Energy Center. The enclosed inspection report documents the inspection findings which were discussed on June 03, 2005, with Mr. J. Bjorseth and other members of your staff.
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The purpose of this inspection was to assess the safety significance and any necessary regulatory actions associated with the primary system hydrostatic test, VT-2 inspections, and control rod testing activities that occurred at Duane Arnold on April 26 and 27, 2005. Within these areas, the inspection consisted of interviews with personnel and the selected examination of procedures and representative records.
Based upon the results of this inspection, the NRC identified two issues that were evaluated under the risk significance determination process as having very low safety significance (green).
The NRC determined that violations were associated with each of the two issues. One of the issues was also evaluated in accordance with the NRC Enforcement Policy and was determined to be a Severity Level IV violation of NRC requirements. The current Enforcement Policy is included on the NRCs Web site as www.nrc.gov; select What We Do, Enforcement and Enforcement Policy. The violations are cited in the enclosed Notice of Violation (Notice) and the circumstances surrounding the violations are described in detail in the subject inspection report. The violations are being cited in the enclosed Notice because you failed to restore compliance within a reasonable time period after the violations were identified and you failed to enter the issues into your corrective action program to address recurrence. The violations involved your failure to comply with the requirements of Technical Specification 3.10.1, System Leakage and Hydrostatic Testing, and 10 CFR 50.59, Changes, Tests, and Experiments.
You are required to respond to this letter and should follow the instructions specified in the enclosed Notice when preparing your response. The NRC will use your response, in part, to determine whether further enforcement action is necessary to ensure compliance with G. Van Middlesworth-2-
regulatory requirements. During the discussion of the violations at the exit, your staff indicated that they did not agree with the violations, and would include the basis for the disagreement in the response to our Notice of Violation.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosures and your response will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Mark A. Satorius, Director Division of Reactor Projects Docket No. 50-331 License No. DPR-49
Enclosures:
Inspection Report 5000331/2005011 w/Attachment: Supplemental Information Notice of Violation
REGION III==
Docket No:
50-331 License No:
DPR-49 Report No:
05000331/2005011 Licensee:
Nuclear Management Company, LLC Facility:
Duane Arnold Energy Center Location:
3277 DAEC Road Palo, Iowa 52324-9785 Dates:
April 25, 2005 through June 03, 2005 Inspectors:
G. Wilson, Senior Resident Inspector R. Baker, Resident Inspector Approved by:
Bruce L. Burgess, Chief Branch 2 Division of Reactor Projects
Enclosure
SUMMARY OF FINDINGS
IR 05000331/2005000; 04/25/2005 - 06/03/2005; Duane Arnold Energy Center, Outage
Activities.
The report covered inspection activities on issues associated with Non-Nuclear Heat Class 1 System Leakage Pressure Tests. The inspections were conducted by the resident inspectors.
The inspection identified a TS 3.10.1 violation associated with a Green finding and one Severity Level IV violation. The significance of most findings is indicated by their color (Green, White,
Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
A.
Inspector-Identified and Self-Revealed Findings
Cornerstone: Mitigating Systems
- Green.
The inspectors identified that the licensee was not in compliance with Technical Specification 3.10.1, System Leakage and Hydrostatic Testing Operation. The non-compliance occurred when the licensee remained above 212°F to performed SCRAM time testing after completion of the reactor coolant system hydrostatic testing and required VT-2 leakage inspections on April 26 and 27, 2005. Therefore, the operating exemptions allowed by TS 3.10.1 for the system leakage tests would not be applicable.
Because the issue was not entered into your corrective action program and you did not restore compliance within a reasonable period of time, a Notice of Violation is being issued. The finding was determined to be of very low safety significance since the procedure was performed at the end of an outage, when the decay heat rate was very low, and multiple trains of emergency core cooling systems were available for accident purposes. This was determined to be a TS 3.10.1 violation associated with a Green finding. (Section 1R20)
- Green.
The inspectors identified that a change to the procedures for the Non-Nuclear Heat Class 1 System Leakage Pressure Tests required prior NRC approval. The procedural changes lengthened the amount of time that the reactor coolant system would exceed 212°F, an unplanned mode change, and added control rod drive scram time testing. These procedural changes resulted in a need for a change in the Technical Specifications (TS) 3.10.1, System Leakage and Hydrostatic Testing Operation.
The finding involved a violation of 10 CFR 50.59, an activity that may impact the regulatory process. Therefore, the finding was evaluated in accordance with the traditional enforcement process. Because the finding was not entered into your corrective action program and you did not restore compliance within a reasonable period of time, a Notice of Violation is being issued. The finding was determined to be of very low safety significance since the System Leakage Test was performed at the end of the refueling outage when the decay heat rate was very low and multiple trains of emergency core cooling systems were available for accident purposes. This finding was determined to be a Severity Level IV violation of 10 CFR 50.59. (Section 1R20)
Licensee-Identified Violations
No findings of significance were identified.
REPORT DETAILS
REACTOR SAFETY
Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity
1R20 Outage Activities
.1 Refueling Outage
a. Inspection Scope
The inspectors observed outage activities for Scheduled Refueling Outage Number 19 during this inspection period. Outage configuration management was monitored by verifying that the licensee maintained appropriate defense in depth to address all shutdown safety functions and satisfy Technical Specification (TS) requirements. The documents listed in the Attachment were used to accomplish the objectives of the inspection procedure. This inspection will not count as an annual sample.
b. Findings
1. Technical Specification 3.10.1 Compliance
Introduction:
The inspectors identified that the licensee failed to comply with TS 3.10.1 System Leakage and Hydrostatic Testing Operation, requirements. The issue was considered to be of very low safety significance (Green).
Description:
On April 26, 2005, the inspectors identified that the licensee was not in compliance with Special Operations TS 3.10.1, System Leakage and Hydrostatic Testing Operation. The non-compliance was due to the failure to cool down the plant following completion of the reactor coolant system hydro and VT-2 inspections. The licensee extended the operation of the plant with temperatures greater than 212°F to perform SCRAM time testing, which was completed on April 27, 2005. The inspectors questioned the licensees compliance with TS 3.10.1, since the operating exemptions for plant operation only apply for system leakage and hydrostatic testing, therefore the exemptions are not applicable for SCRAM time testing. Because SCRAM time testing was performed after the leakage inspections were complete, the operating exemptions allowed by TS 3.10.1 for system leakage tests would not be applicable. During the extension of the time that the plant was greater than 212°F for SCRAM time testing, the plant would be considered to be in Mode 3 without having all the requirements necessary for Mode 3 operation. The inspectors first questioned the licensees TS compliance on April 26, 2005 during a discussion with the Operations Shift Manager.
Additional discussions with the licensee occurred on April 27, 2005, and involved the Site Director, Plant Manager, and the Regulatory Affairs Manager. Even though the inspectors challenged the compliance with TS 3.10.1, the licensee continued to perform SCRAM time testing until it was completed and then commenced a plant cool down. No actions were performed to resolve the non-compliance. Upon further evaluation, the inspectors identified that the licensee had also violated the requirements of TS 3.10.1 to perform SCRAM time testing during the Class 1 System Leakage Pressure Test for the following periods: November 23, 1999, through November 25, 1999, May 18, 2001, through May 21, 2001, and April 15, 2003, through April 16, 2003.
Analysis:
Using IMC 0612, Power Reactor Inspection Reports, the inspectors determined that the failure to comply with TS 3.10.1 was a failure to meet a requirement and was reasonably in the licensees ability to foresee, therefore it was a performance deficiency. Since a performance deficiency existed, the inspectors reviewed this issue against the guidance contained in Appendix B, Issue Dispositioning Screening, of IMC 0612. In particular, the inspectors compared this finding to the findings identified in Appendix E, Examples of Minor Issues, of IMC 0612 to determine if the finding was more than minor. Following that review, the inspectors concluded that the guidance in Appendix E was not applicable for the specific finding. As a result, the inspectors compared this performance deficiency to the minor questions contained in Appendix B of IMC 0612. The inspectors determined that the issue was more than minor because the condition could be reasonably viewed as a precursor to a significant event. The precursor to a significant event was based on the fact that the Mode of plant operation was changed without having met all the necessary requirements for the operability of emergency core cooling systems (ECCS).
As a result, the inspectors reviewed this issue in accordance with IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations. The inspectors determined that the issue could not be evaluated using the operating plant SDP because the plant was in a shutdown condition. Therefore the inspectors evaluated the issue utilizing the associated plant condition and available mitigating equipment.
Since the issue occurred at the end of the refueling outage, the resultant decay heat load of the fuel was very low. In addition, multiple trains of emergency core cooling systems were available for accident purposes, therefore the issue was of very low safety significance (Green).
Enforcement:
Special Operations TS 3.10.1, System Leakage and Hydrostatic Testing, allows exemptions of reactor coolant temperature requirements for the performance of system leakage and hydrostatic testing. The exemptions allows the plant to go above 212°F and still be considered in Mode 4 even though the associated temperature would be Mode 3 for system leakage tests. Contrary to this requirement, the licensee extended the plant operation time with reactor coolant temperature greater than 212°F from April 26 through April 27, 2005, to perform SCRAM time testing following the completion of the VT-2 inspections for the systems leakage test. Furthermore, the licensee failed to restore compliance within a reasonable period of time after the issue was identified to your staff on April 26, 2005. In addition, the licensee also failed to comply with the requirements of TS 3.10.1 during the following periods: November 23, 1999, through November 25,1999, May 18, 2001, through May 21, 2001, and April 15, 2003, through April 16, 2003. The failure to comply with the requirements of TS 3.10.1 was a violation.
Since the licensee failed to restore compliance within a reasonable time after the violation was identified and they did not place the violation into a corrective action program to prevent recurrence, a Notice of Violation (NOV) is being issued for this violation associated with a Green finding, consistent with Section VI.A.1 of the NRC Enforcement Policy. (NOV 05000331/2005011-01)
Procedures Changes for Non-Nuclear Heat Class 1 System Leakage Pressure Tests
Introduction:
The inspectors identified that the licensee failed to obtain prior NRC approval in accordance with 10 CFR 50.59, Changes, tests, and experiments, for a change to the Procedures for Non-Nuclear Heat Class 1 System Leakage Pressure Tests. The issue was considered to be of very low safety significance (Green) and was dispositioned as a Severity Level IV violation.
Description:
On April 27, 2005, the inspectors identified that an inadequate 10 CFR 50.59 screening was performed in 1999 for the procedure changes associated with the Surveillance Test Procedure (STP) 3.10.1.01, Non-Nuclear Heat Class 1 System Leakage Pressure Tests, and STP 3.10.1-02, Non-Nuclear Heat Class 1 Ten Year System Leakage Pressure Test. The licensee performed the 50.59 screening on August 19, 1999, for the procedure changes that were made to STP 3.10.1.01 and STP 3.10.1-02. In that screening, the licensee stated the procedure change did not require a change to the Technical Specifications. Part of the procedure changes associated with the 50.59 screening added steps to hold the reactor pressure at 850-950 pounds per square inch gauge (psig) after the completion of the reactor system hydrostatic test and the Visual Test (VT) - 2 inspections to allow performance of SCRAM time testing. The inspectors questioned the licensees 50.59 screening conclusions since Special Operations TS 3.10.1, System Leakage and Hydrostatic Testing Operation, conditions for operation only apply for system leakage and hydrostatic testing, so the operating exemptions that are given for plant operation greater than 212°F are only applicable for the completion of the leakage inspections and associated plant cooldown.
Since the change added SCRAM time testing after the leakage inspections were complete, the operating exemptions allowed by TS 3.10.1 for System Leakage tests would not be applicable. Therefore, during the extension of the time that the plant was greater than 212°F, which is Mode 3, for SCRAM time testing, the plant would be considered to be in Mode 3 without having all the requirements necessary for Mode 3 operation. The procedure change resulted in a need for a change of TS 3.10.1 to allow the procedure to be performed as written, therefore, in accordance with 10 CFR 50.59, the licensee needed to obtain NRC approval prior to implementing the procedure change.
Analysis:
The violation identified above has existed since 1999, involved an inadequate 10 CFR 50.59 evaluation, and impacted the NRC regulatory process. Therefore this violation is being dispositioned using the traditional enforcement process instead of the significance determination process (SDP). Typically, the Severity Level would be assigned after consideration of appropriate factors for the particular regulatory process violation in accordance with the NRC Enforcement Policy. However, the SDP is also used, if applicable, in order to consider the associated risk significance of the finding prior to assigning a severity level.
Using Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, the inspectors determined that the failure to perform an adequate 50.59 screening evaluation for the procedure changes associated with STP 3.10.1-01 and STP 3.10.1-02 was a failure to meet a requirement and standard therefore it was a performance deficiency.
Since a performance deficiency existed, the inspectors reviewed this issue against the guidance contained in Appendix B, Issue Dispositioning Screening, of IMC 0612. In particular, the inspectors compared this finding to the findings identified in Appendix E, Examples of Minor Issues, of IMC 0612 to determine whether the finding was minor.
Following that review, the inspectors concluded that the guidance in Appendix E was not applicable for the specific finding. As a result, the inspectors compared this performance deficiency to the minor questions contained in Appendix B of IMC 0612. The inspectors determined that the issue was more than minor because the condition could be reasonably viewed as a precursor to a significant event. The precursor to a significant event was based on the fact that the Mode of plant operation was changed without having met all the necessary requirements for the operability of emergency core cooling systems.
As a result, the inspectors reviewed this issue in accordance with IMC 0609, Appendix A, Significance Determination of Reactor Inspection Findings for At-Power Situations. The inspectors determined that the issue could not be evaluated by the associated SDP.
Therefore the inspectors evaluated the issue utilizing the associated plant condition and available mitigating equipment. Since the issue occurred at the end of the refueling outage, the resultant decay heat load of the fuel was very low. In addition, multiple trains of emergency core cooling systems were available for accident purposes, therefore the issue was of considered to have very low safety significance (Green).
Enforcement:
10 CFR 50.59, Changes, tests, and experiments, states, in part, the holder of a license authorizing operation of a production or utilization facility may conduct tests not described in the safety analysis report, without prior Commission approval, unless the proposed test involves a change in the technical specifications incorporated in the license. Contrary to this, on August 19, 1999, the licensee implemented a change to STP 3.10.1.01 and STP 3.10.1-02 which resulted in the need for a change in the TS. The result of the violation was determined to be of very low safety significance; therefore, this violation of 10 CFR 50.59 was classified as a Severity Level IV violation. Since the licensee failed to restore compliance within a reasonable time after the violation was identified and they did not place the violation into a corrective action program to prevent recurrence, a Notice of Violation (NOV) is being issued for this Severity Level IV violation, consistent with Section VI.A.1 of the NRC Enforcement Policy.
4OA6 Meetings
1. Exit Meeting
The inspectors presented the inspection results to Mr. J. Bjorseth and other members of licensee management on June 03, 2005. During the discussion of the violations at the exit, your staff indicated that they did not agree with the violations, and would include the basis for the disagreement in the response to our Notice of Violation. The inspectors asked the licensee whether any materials examined during the inspection should be considered proprietary. No proprietary information was identified.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- G. Van Middlesworth, Site Vice President
- J. Bjorseth, Site Director
- S. Catron, Regulatory Affairs Manager
- D. Curtland, Plant Manager
- G. Rushworth, Operations Manager
Nuclear Regulatory Commission
- B. Burgess, Chief, Division of Reactor Projects, Branch 2
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
- 05000331/2005011-01 NOV Failure to Comply with the Requirements of TS 3.10.1 during the Performance of the Non-Nuclear Heat Class 1 System Leakage Pressure Test
- 05000331/2005011-02 NOV Failure to Comply with the Requirements of 10 CFR 50.59 for a Change to the Procedures for Non-Nuclear Heat Class System Leakage Pressure Tests
Closed
None.
Discussed
None.