IR 05000269/2007005: Difference between revisions
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{{#Wiki_filter: | {{#Wiki_filter:January 31, 2008 | ||
==SUBJECT:== | ==SUBJECT:== | ||
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Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Oconee facility. | Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Oconee facility. | ||
DPC | DPC | ||
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | |||
Sincerely, | Sincerely, | ||
/RA/ | /RA/ | ||
James H. Moorman, III Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.: 50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55 | James H. Moorman, III Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.: | ||
50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55 | |||
===Enclosure:=== | ===Enclosure:=== | ||
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REGION II== | REGION II== | ||
Docket Nos: 50-269, 50-270, 50-287 License Nos: DPR-38, DPR-47, DPR-55 Report No: 05000269/2007005, 05000270/2007005, 05000287/2007005 Licensee: Duke Power Company LLC Facility: Oconee Nuclear Station, Units 1, 2, and 3 Location: 7800 Rochester Highway Seneca, SC 29672 Dates: October 1, 2007 - December 31, 2007 Inspectors: D. Rich, Senior Resident Inspector A. Hutto, Resident Inspector E. Riggs, Resident Inspector A. Vargas-Mendez, Reactor Inspector (Sections 1R08, 4OA7) | Docket Nos: | ||
50-269, 50-270, 50-287 License Nos: | |||
DPR-38, DPR-47, DPR-55 Report No: | |||
05000269/2007005, 05000270/2007005, 05000287/2007005 Licensee: | |||
Duke Power Company LLC Facility: | |||
Oconee Nuclear Station, Units 1, 2, and 3 Location: | |||
7800 Rochester Highway Seneca, SC 29672 Dates: | |||
October 1, 2007 - December 31, 2007 Inspectors: | |||
D. Rich, Senior Resident Inspector A. Hutto, Resident Inspector E. Riggs, Resident Inspector A. Vargas-Mendez, Reactor Inspector (Sections 1R08, 4OA7) | |||
M. Coursey, Reactor Inspector (Sections 1R08, 4OA7) | M. Coursey, Reactor Inspector (Sections 1R08, 4OA7) | ||
Approved by: James H. Moorman, III, Chief Reactor Projects Branch 1 Division of Reactor Projects Enclosure | Approved by: | ||
James H. Moorman, III, Chief Reactor Projects Branch 1 Division of Reactor Projects | |||
Enclosure | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
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===NRC Identified and Self-Revealing Findings=== | ===NRC Identified and Self-Revealing Findings=== | ||
===Cornerstone: Initiating Events=== | ===Cornerstone: Initiating Events=== | ||
* | |||
: '''Green.''' | : '''Green.''' | ||
A self-revealing non-cited violation (NCV) of Technical Specification (TS)5.4.1 was identified for failure to establish and implement an adequate procedure for loss of the Unit 3 spent fuel pool (SFP) cooling and/or level. More specifically, | A self-revealing non-cited violation (NCV) of Technical Specification (TS)5.4.1 was identified for failure to establish and implement an adequate procedure for loss of the Unit 3 spent fuel pool (SFP) cooling and/or level. More specifically, | ||
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===Cornerstone: Barrier Integrity=== | ===Cornerstone: Barrier Integrity=== | ||
* | |||
: '''Green.''' | : '''Green.''' | ||
The inspectors identified an NCV of TS 5.4.1 for the failure to establish and implement adequate procedures for containment closure following a potential loss of decay heat removal (LDHR) event. More specifically, existing procedures did not adequately address control of vehicles blocking the equipment hatch opening, as was the case on October 31, 2007. | The inspectors identified an NCV of TS 5.4.1 for the failure to establish and implement adequate procedures for containment closure following a potential loss of decay heat removal (LDHR) event. More specifically, existing procedures did not adequately address control of vehicles blocking the equipment hatch opening, as was the case on October 31, 2007. | ||
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===Licensee-Identified Violations=== | ===Licensee-Identified Violations=== | ||
Two violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations are listed in Section 4OA7. | Two violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations are listed in Section 4OA7. | ||
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Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity | Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity | ||
{{a|1R01}} | {{a|1R01}} | ||
==1R01 Adverse Weather Protection | |||
==1R01 Adverse Weather Protection | |||
Cold Weather Preparations | Cold Weather Preparations | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed the licensees preparations for adverse weather associated with cold ambient temperatures for the three risk significant systems listed below. This included field walkdowns to assess the material condition and operation of freeze protection equipment (e.g., heat tracing, instrument box heaters, area space heaters, etc.), as well as other preparations made to protect plant equipment from freeze conditions. In addition, the inspectors conducted discussions with operations, engineering, and maintenance personnel responsible for implementing the licensees cold weather protection program to assess the licensees ability to identify and resolve deficient conditions associated with cold weather protection equipment prior to cold weather events. Documents reviewed during this inspection are listed in the Attachment to this report. | The inspectors reviewed the licensees preparations for adverse weather associated with cold ambient temperatures for the three risk significant systems listed below. This included field walkdowns to assess the material condition and operation of freeze protection equipment (e.g., heat tracing, instrument box heaters, area space heaters, etc.), as well as other preparations made to protect plant equipment from freeze conditions. In addition, the inspectors conducted discussions with operations, engineering, and maintenance personnel responsible for implementing the licensees cold weather protection program to assess the licensees ability to identify and resolve deficient conditions associated with cold weather protection equipment prior to cold weather events. Documents reviewed during this inspection are listed in the Attachment to this report. | ||
* Essential Siphon Vacuum System | * Essential Siphon Vacuum System | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R04}} | No findings of significance were identified. {{a|1R04}} | ||
==1R04 Equipment Alignment | |||
== | |||
===.1 Partial Walkdown=== | ===.1 Partial Walkdown=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors conducted partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems while the other train or system was inoperable or out-of-service (OOS). The walkdowns included, as appropriate, reviews of plant procedures and other documents to determine correct system lineups, and verification of critical components to identify any discrepancies which could affect operability of the redundant train or backup system. Documents reviewed are listed in the Attachment to this report. The following three systems were included in this review: | The inspectors conducted partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems while the other train or system was inoperable or out-of-service (OOS). The walkdowns included, as appropriate, reviews of plant procedures and other documents to determine correct system lineups, and verification of critical components to identify any discrepancies which could affect operability of the redundant train or backup system. Documents reviewed are listed in the Attachment to this report. The following three systems were included in this review: | ||
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===.2 Complete Walkdown of the Unit 3 Emergency Feedwater System (EFW)=== | ===.2 Complete Walkdown of the Unit 3 Emergency Feedwater System (EFW)=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a system walkdown on accessible portions of the Unit 3 EFW system. The inspectors focused on verifying proper valve and breaker positioning, power availability, no damage to piping or cable tray structural supports, and material condition. | The inspectors performed a system walkdown on accessible portions of the Unit 3 EFW system. The inspectors focused on verifying proper valve and breaker positioning, power availability, no damage to piping or cable tray structural supports, and material condition. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R05}} | No findings of significance were identified. {{a|1R05}} | ||
Fire Area Walkdowns | ==1R05 Fire Protection Fire Area Walkdowns | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors conducted tours in eleven areas of the plant to verify that combustibles and ignition sources were properly controlled, and that fire detection and suppression capabilities were intact. The inspectors selected the areas based on a review of the licensees safe shutdown analysis and the probabilistic risk assessment based sensitivity studies for fire-related core damage sequences. Documents reviewed are listed in the Attachment to this report. Inspections of the following areas were conducted during this inspection period: | The inspectors conducted tours in eleven areas of the plant to verify that combustibles and ignition sources were properly controlled, and that fire detection and suppression capabilities were intact. The inspectors selected the areas based on a review of the licensees safe shutdown analysis and the probabilistic risk assessment based sensitivity studies for fire-related core damage sequences. Documents reviewed are listed in the Attachment to this report. Inspections of the following areas were conducted during this inspection period: | ||
* Unit 1 and 2 Low Pressure Injection (LPI) Pump Rooms (3) | * Unit 1 and 2 Low Pressure Injection (LPI) Pump Rooms (3) | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R06}} | No findings of significance were identified. {{a|1R06}} | ||
==1R06 Flood Protection Measures (Internal) | |||
==1R06 Flood Protection Measures (Internal) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed the licensees turbine building flood control measures while performing Unit 3 condenser maintenance during its refueling outage commencing in October 2007. The inspectors determined that the licensee complied with the applicable Unit 1 waterbox and condenser circulating water (CCW) inlet and outlet de-watering and watering operating procedures (OP/1/A/1104/012 E and G). The inspectors also walked down the appropriate CCW valve isolations to verify that they were established per Selected Licensee Commitments 16.9.11. | The inspectors reviewed the licensees turbine building flood control measures while performing Unit 3 condenser maintenance during its refueling outage commencing in October 2007. The inspectors determined that the licensee complied with the applicable Unit 1 waterbox and condenser circulating water (CCW) inlet and outlet de-watering and watering operating procedures (OP/1/A/1104/012 E and G). The inspectors also walked down the appropriate CCW valve isolations to verify that they were established per Selected Licensee Commitments 16.9.11. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R08}} | No findings of significance were identified. {{a|1R08}} | ||
==1R08 Inservice Inspection (ISI) Activities | |||
== | |||
===.1 Piping Systems ISI=== | ===.1 Piping Systems ISI=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
From November 5-16, 2007, the inspectors reviewed the implementation of the licensees ISI program for monitoring degradation of the reactor coolant system (RCS)boundary and risk significant piping system boundaries. The inspectors reviewed a sample from activities performed during the Unit 3 Fall 2007 refueling outage including non-destructive examinations (NDE) required by the 1998 Edition, 2000 Addenda, of American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code, Section XI, and augmented examination commitments. | From November 5-16, 2007, the inspectors reviewed the implementation of the licensees ISI program for monitoring degradation of the reactor coolant system (RCS)boundary and risk significant piping system boundaries. The inspectors reviewed a sample from activities performed during the Unit 3 Fall 2007 refueling outage including non-destructive examinations (NDE) required by the 1998 Edition, 2000 Addenda, of American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code, Section XI, and augmented examination commitments. | ||
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===.2 Boric Acid Corrosion Control (BACC) Program=== | ===.2 Boric Acid Corrosion Control (BACC) Program=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the licensees Boric Acid Corrosion Control (BACC) program to ensure compliance with commitments made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants. | The inspectors reviewed the licensees Boric Acid Corrosion Control (BACC) program to ensure compliance with commitments made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants. | ||
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===.3 Steam Generator (SG) Tube ISI=== | ===.3 Steam Generator (SG) Tube ISI=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the SG examination scope, expansion criteria, eddy current testing (ET) acquisition procedures, ET analysis procedures, the SG Operational Assessment, in-situ tube pressure testing procedures, and records and examination reports to confirm that: | The inspectors reviewed the SG examination scope, expansion criteria, eddy current testing (ET) acquisition procedures, ET analysis procedures, the SG Operational Assessment, in-situ tube pressure testing procedures, and records and examination reports to confirm that: | ||
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===.4 Identification and Resolution of Problems=== | ===.4 Identification and Resolution of Problems=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a review of SG and ISI-related problems that were identified by the licensee and entered into the corrective action program. The inspectors reviewed these corrective action program documents to confirm that the licensee had appropriately described the scope of the problems. In addition, the inspectors review included confirmation that the licensee had an appropriate threshold for identifying issues and had implemented effective corrective actions. The inspectors evaluated the threshold for identifying issues through interviews with licensee staff and review of licensee actions to incorporate lessons learned from industry issues related to the ISI program. The inspectors performed these reviews to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. | The inspectors performed a review of SG and ISI-related problems that were identified by the licensee and entered into the corrective action program. The inspectors reviewed these corrective action program documents to confirm that the licensee had appropriately described the scope of the problems. In addition, the inspectors review included confirmation that the licensee had an appropriate threshold for identifying issues and had implemented effective corrective actions. The inspectors evaluated the threshold for identifying issues through interviews with licensee staff and review of licensee actions to incorporate lessons learned from industry issues related to the ISI program. The inspectors performed these reviews to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R11}} | No findings of significance were identified. {{a|1R11}} | ||
Simulator Training | ==1R11 Licensed Operator Requalification Simulator Training | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors observed licensed operator simulator training on October 19, 2007. The scenario involved training on emergency operating procedure rules one through five. | The inspectors observed licensed operator simulator training on October 19, 2007. The scenario involved training on emergency operating procedure rules one through five. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R12}} | No findings of significance were identified. {{a|1R12}} | ||
==1R12 Maintenance Effectiveness | |||
==1R12 Maintenance Effectiveness | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed the licensees effectiveness in performing routine maintenance activities. This review included an assessment of the licensees practices pertaining to the identification, scoping, and handling of degraded equipment conditions, as well as common cause failure evaluations. For each item selected, the inspectors performed a detailed review of the problem history and surrounding circumstances, evaluated the extent of condition reviews as required, and reviewed the generic implications of the equipment and/or work practice problem. For those structures, systems, and components (SSCs) scoped in the maintenance rule, the inspectors verified that reliability and unavailability were properly monitored and that 10 CFR 50.65 (a)(1) and (a)(2) classifications were justified in light of the reviewed degraded equipment condition. The inspectors reviewed the following items: | The inspectors reviewed the licensees effectiveness in performing routine maintenance activities. This review included an assessment of the licensees practices pertaining to the identification, scoping, and handling of degraded equipment conditions, as well as common cause failure evaluations. For each item selected, the inspectors performed a detailed review of the problem history and surrounding circumstances, evaluated the extent of condition reviews as required, and reviewed the generic implications of the equipment and/or work practice problem. For those structures, systems, and components (SSCs) scoped in the maintenance rule, the inspectors verified that reliability and unavailability were properly monitored and that 10 CFR 50.65 (a)(1) and (a)(2) classifications were justified in light of the reviewed degraded equipment condition. The inspectors reviewed the following items: | ||
* PIP O-07-4674, 2A High Pressure Injection Pump Shaft/Seal Overheating Due to Throttle Bushing Contact | * PIP O-07-4674, 2A High Pressure Injection Pump Shaft/Seal Overheating Due to Throttle Bushing Contact | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R13}} | No findings of significance were identified. {{a|1R13}} | ||
==1R13 Maintenance Risk Assessment and Emergent Work Evaluations | |||
==1R13 Maintenance Risk Assessment and Emergent Work Evaluations | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
For the six selected SSCs and activities listed below, the inspectors evaluated the following attributes: | For the six selected SSCs and activities listed below, the inspectors evaluated the following attributes: | ||
: (1) the effectiveness of the risk assessments performed before maintenance activities were conducted; | : (1) the effectiveness of the risk assessments performed before maintenance activities were conducted; | ||
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====b. Findings==== | ====b. Findings==== | ||
Inspectors noted one licensee identified violation associated with PIP O-07-5829, which | Inspectors noted one licensee identified violation associated with PIP O-07-5829, which is documented in Section 4OA7 of this report. | ||
{{a|1R15}} | {{a|1R15}} | ||
==1R15 Operability Evaluations | |||
==1R15 Operability Evaluations | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed selected operability evaluations affecting risk significant systems, to assess, as appropriate: | The inspectors reviewed selected operability evaluations affecting risk significant systems, to assess, as appropriate: | ||
: (1) the technical adequacy of the evaluations; | : (1) the technical adequacy of the evaluations; | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R19}} | No findings of significance were identified. {{a|1R19}} | ||
==1R19 Post-Maintenance Testing (PMT) | |||
==1R19 Post-Maintenance Testing (PMT) | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed PMT procedures and/or test activities, as appropriate, for selected risk significant systems to assess whether: | The inspectors reviewed PMT procedures and/or test activities, as appropriate, for selected risk significant systems to assess whether: | ||
: (1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel; | : (1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel; | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R20}} | No findings of significance were identified. {{a|1R20}} | ||
==1R20 Refueling & Outage Activities | |||
==1R20 Refueling & Outage Activities | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors conducted reviews and observations for selected outage activities to ensure that: | The inspectors conducted reviews and observations for selected outage activities to ensure that: | ||
: (1) the licensee considered risk in developing the outage plan; | : (1) the licensee considered risk in developing the outage plan; | ||
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====b. Findings==== | ====b. Findings==== | ||
: (1) Inadequate Loss of Spent Fuel Pool Cooling Abnormal Procedure | : (1) Inadequate Loss of Spent Fuel Pool Cooling Abnormal Procedure | ||
=====Introduction:===== | =====Introduction:===== | ||
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===1. For RV head lifts occurring during and after April, 2007, the licensee=== | ===1. For RV head lifts occurring during and after April, 2007, the licensee=== | ||
implemented load handling procedures consistent with the existing load drop analysis. | |||
implemented load handling procedures consistent with the existing load drop | |||
===2. Inspections of the following areas revealed no findings of significance:=== | ===2. Inspections of the following areas revealed no findings of significance:=== | ||
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Therefore, consistent with the intent of EGM 07-006, the NRC is exercising enforcement discretion (EA-08-037) for the above violation in accordance with Section VII.B.6 of the NRC Enforcement Policy without any enforcement action. | Therefore, consistent with the intent of EGM 07-006, the NRC is exercising enforcement discretion (EA-08-037) for the above violation in accordance with Section VII.B.6 of the NRC Enforcement Policy without any enforcement action. | ||
{{a|1R22}} | {{a|1R22}} | ||
==1R22 Surveillance Testing | |||
==1R22 Surveillance Testing | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors witnessed surveillance tests and/or reviewed test data of the five risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met TS, the UFSAR, and licensee procedure requirements. In addition, the inspectors determined if the testing effectively demonstrated that the SSCs were ready and capable of performing their intended safety functions. Documents reviewed are listed in the to this report. | The inspectors witnessed surveillance tests and/or reviewed test data of the five risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met TS, the UFSAR, and licensee procedure requirements. In addition, the inspectors determined if the testing effectively demonstrated that the SSCs were ready and capable of performing their intended safety functions. Documents reviewed are listed in the to this report. | ||
* PT/1/A/0600/012, Unit 1 Turbine Driven Emergency Feedwater Pump Test (IST) | * PT/1/A/0600/012, Unit 1 Turbine Driven Emergency Feedwater Pump Test (IST) | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. {{a|1R23}} | No findings of significance were identified. {{a|1R23}} | ||
==1R23 Temporary Plant Modifications | |||
==1R23 Temporary Plant Modifications | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed documents and observed portions of the installation of two selected temporary modifications. Among the documents reviewed were system design bases, the UFSAR, TS, system operability/availability evaluations, and the 10 CFR 50.59 screening. As appropriate, the inspectors determined if: the installation was consistent with the modification documents; it was in accordance with the configuration control process; adequate procedures and changes were made; and post installation testing was adequate. The following items were reviewed under this inspection procedure: | The inspectors reviewed documents and observed portions of the installation of two selected temporary modifications. Among the documents reviewed were system design bases, the UFSAR, TS, system operability/availability evaluations, and the 10 CFR 50.59 screening. As appropriate, the inspectors determined if: the installation was consistent with the modification documents; it was in accordance with the configuration control process; adequate procedures and changes were made; and post installation testing was adequate. The following items were reviewed under this inspection procedure: | ||
* OD 500822, Installation and Removal of CCW Discharge RTDs | * OD 500822, Installation and Removal of CCW Discharge RTDs | ||
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==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
{{a|4OA1}} | {{a|4OA1}} | ||
==4OA1 Performance Indicator (PI) Verification== | ==4OA1 Performance Indicator (PI) Verification== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors verified the Mitigating Systems Performance Indicators (MSPI) listed in the table below (for all three units), to determine its accuracy and completeness against requirements in NEI 99-02, Regulatory Assessment Performance Indicator Guideline. | The inspectors verified the Mitigating Systems Performance Indicators (MSPI) listed in the table below (for all three units), to determine its accuracy and completeness against requirements in NEI 99-02, Regulatory Assessment Performance Indicator Guideline. | ||
===Cornerstone: Mitigating Systems=== | ===Cornerstone: Mitigating Systems=== | ||
Performance Indicator Verification Period Records Reviewed MSPI | |||
Performance Indicator | - high pressure injection | ||
- emergency feedwater | |||
- emergency AC power | |||
- residual heat removal | |||
- support cooling water 4th quarter, 2006; 1st, 2nd, and 3rd quarter, 2007 | |||
* Operating Logs, Train Unavailability Data | |||
* Maintenance Records | * Maintenance Records | ||
* Maintenance Rule Data | * Maintenance Rule Data | ||
* Corrective Action Program | * Corrective Action Program | ||
* Consolidated Data Entry Derivation Reports | * Consolidated Data Entry Derivation Reports | ||
* System Health Reports | * System Health Reports | ||
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No findings of significance were identified. | No findings of significance were identified. | ||
{{a|4OA2}} | {{a|4OA2}} | ||
==4OA2 Identification and Resolution of Problems== | ==4OA2 Identification and Resolution of Problems== | ||
===.1 Daily Screening of Corrective Action Reports=== | ===.1 Daily Screening of Corrective Action Reports=== | ||
As required by Inspection Procedure (IP) 71152, "Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed daily screening of items entered into the licensees corrective action program. This screening was accomplished by reviewing copies of PIPs, attending daily screening meetings, and accessing the licensees computerized database. | As required by Inspection Procedure (IP) 71152, "Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed daily screening of items entered into the licensees corrective action program. This screening was accomplished by reviewing copies of PIPs, attending daily screening meetings, and accessing the licensees computerized database. | ||
===.2 Semi-Annual Trend Review=== | ===.2 Semi-Annual Trend Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
As required by IP 71152, "Identification and Resolution of Problems," the inspectors performed a review of the licensees Corrective Action Program (CAP) and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screenings discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six month period of July 2007 through December 2007, although some examples expanded beyond those dates when the scope of the trend warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, plant health team vulnerability lists, focus area reports, system health reports, self-assessment reports, maintenance rule reports, and Safety Review Group Monthly Reports. The inspectors compared and contrasted their results with the results contained in the licensees latest quarterly trend reports. | As required by IP 71152, "Identification and Resolution of Problems," the inspectors performed a review of the licensees Corrective Action Program (CAP) and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screenings discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six month period of July 2007 through December 2007, although some examples expanded beyond those dates when the scope of the trend warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, plant health team vulnerability lists, focus area reports, system health reports, self-assessment reports, maintenance rule reports, and Safety Review Group Monthly Reports. The inspectors compared and contrasted their results with the results contained in the licensees latest quarterly trend reports. | ||
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Corrective actions associated with a sample of the issues identified in the licensees trend report were reviewed for adequacy. | Corrective actions associated with a sample of the issues identified in the licensees trend report were reviewed for adequacy. | ||
b. Assessment and Observations No findings of significance were identified. In general, the licensee has identified trends and has appropriately addressed the trends with their CAP. | b. | ||
Assessment and Observations No findings of significance were identified. In general, the licensee has identified trends and has appropriately addressed the trends with their CAP. | |||
===.3 Focused Review=== | ===.3 Focused Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed an in-depth review of one issue entered into the licensees CAP, and also performed an in-depth review of existing plant operator workarounds. | The inspectors performed an in-depth review of one issue entered into the licensees CAP, and also performed an in-depth review of existing plant operator workarounds. | ||
| Line 471: | Line 498: | ||
No findings of significance were identified. | No findings of significance were identified. | ||
{{a|4OA3}} | {{a|4OA3}} | ||
==4OA3 Event Followup== | ==4OA3 Event Followup== | ||
(Closed) Licensee Event Report (LER) 05000269/2007002-00, Cask Shipments Include Startup Neutron Sources Not Listed in Certificate of Compliance (COC). This issue concerned a shipment of spent fuel from Oconee to McGuire in 1987 which included two startup neutron sources. Shipping fuel assemblies with a startup source violated shipping cask COC Number 9015, Revision 13. The issue was identified by the licensee and adequately addressed in the corrective action program under PIPs M-07-5072, O-06-4569, and G-95-0896. This failure to comply with the COC constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section IV of the NRC's Enforcement Policy. This LER is closed. | |||
{{a|4OA6}} | |||
==4OA6 Management Meetings (Including Exit Meeting)== | ==4OA6 Management Meetings (Including Exit Meeting)== | ||
===.1=== | |||
===.1 Exit Meeting Summary=== | ===Exit Meeting Summary=== | ||
The inspectors presented the inspection results to Mr. M. Glover, Oconee Station Manager, and other members of licensee management at the conclusion of the inspection on January 9, 2008. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified. | The inspectors presented the inspection results to Mr. M. Glover, Oconee Station Manager, and other members of licensee management at the conclusion of the inspection on January 9, 2008. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified. | ||
===.2 Regulatory Performance Meeting=== | ===.2 Regulatory Performance Meeting=== | ||
A public Regulatory Performance Meeting was held on December 5, 2007, at the Oconee World of Energy Visitor Center. The purpose of this meeting was to discuss the performance deficiencies, lessons learned, and the proposed corrective actions associated with the two White findings and the White performance indicator in the Mitigating Systems Cornerstone that resulted in the performance of all three Oconee Units being in the Degraded Cornerstone Column of the NRCs Action Matrix from the fourth quarter 2006 to the third quarter 2007. The required supplemental inspection of these three White issues was completed on August 31, 2007, and the results were reported in NRC Supplemental Inspection Report 05000269,270,287/2007009, dated October 12, 2007. Meeting attendees are listed in the Attachment below. | A public Regulatory Performance Meeting was held on December 5, 2007, at the Oconee World of Energy Visitor Center. The purpose of this meeting was to discuss the performance deficiencies, lessons learned, and the proposed corrective actions associated with the two White findings and the White performance indicator in the Mitigating Systems Cornerstone that resulted in the performance of all three Oconee Units being in the Degraded Cornerstone Column of the NRCs Action Matrix from the fourth quarter 2006 to the third quarter 2007. The required supplemental inspection of these three White issues was completed on August 31, 2007, and the results were reported in NRC Supplemental Inspection Report 05000269,270,287/2007009, dated October 12, 2007. Meeting attendees are listed in the Attachment below. | ||
{{a|4OA7}} | {{a|4OA7}} | ||
==4OA7 Licensee Identified Violations== | ==4OA7 Licensee Identified Violations== | ||
The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a NCVs. | The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a NCVs. | ||
* 10 CFR Part 50.65 (a)(4), requires, in part, that prior to performing maintenance activities, the licensee assess the potential risk increase resulting from the proposed maintenance activities. Contrary to the above, on October 21, 2007, the licensee failed to adequately assess the risk associated with activities to pressurize the Unit 3 Reactor Building (RB) while the 3A LPI cooler was OOS for maintenance. On October 22, 2007, the licensee identified and corrected the inadequate risk assessment, which changed the units risk profile from Yellow to Orange. The licensee halted activities to pressurize the U3 RB, which returned the units risk profile to Yellow. In accordance with Inspection Manual Chapter (IMC) 0612 Appendix B, Issue Screening and Appendix E, Examples of Minor Issues, Section 7. Maintenance Rule Issues, Example e., the issue was determined to be more than minor. This finding is of very low safety significance because the incremental core damage probability was determined to be zero, and the incremental large early release probability was determined to be less than 1.2 E-9. This finding was documented in the licensees corrective action program as PIP O-07-5829. | * 10 CFR Part 50.65 (a)(4), requires, in part, that prior to performing maintenance activities, the licensee assess the potential risk increase resulting from the proposed maintenance activities. Contrary to the above, on October 21, 2007, the licensee failed to adequately assess the risk associated with activities to pressurize the Unit 3 Reactor Building (RB) while the 3A LPI cooler was OOS for maintenance. On October 22, 2007, the licensee identified and corrected the inadequate risk assessment, which changed the units risk profile from Yellow to Orange. The licensee halted activities to pressurize the U3 RB, which returned the units risk profile to Yellow. In accordance with Inspection Manual Chapter (IMC) 0612 Appendix B, Issue Screening and Appendix E, Examples of Minor Issues, Section 7. Maintenance Rule Issues, Example e., the issue was determined to be more than minor. This finding is of very low safety significance because the incremental core damage probability was determined to be zero, and the incremental large early release probability was determined to be less than 1.2 E-9. This finding was documented in the licensees corrective action program as PIP O-07-5829. | ||
| Line 500: | Line 526: | ||
==KEY POINTS OF CONTACT== | ==KEY POINTS OF CONTACT== | ||
Licensee | Licensee | ||
: [[contact::E. Anderson]], Superintendent of Operations | : [[contact::E. Anderson]], Superintendent of Operations | ||
* | * | ||
: [[contact::S. Batson]], Engineering Manager | : [[contact::S. Batson]], Engineering Manager | ||
* | * | ||
: [[contact::D. Baxter]], Site Vice President | : [[contact::D. Baxter]], Site Vice President | ||
| Line 513: | Line 538: | ||
: [[contact::S. Capps]], Mechanical and Civil Engineering Manager | : [[contact::S. Capps]], Mechanical and Civil Engineering Manager | ||
: [[contact::N. Constance]], Operations Training Manager | : [[contact::N. Constance]], Operations Training Manager | ||
: [[contact::C. Curry]], Mechanical/Civil Engineering Manager | : [[contact::C. Curry]], Mechanical/Civil Engineering Manager | ||
: [[contact::P. Culbertson]], Maintenance Manager | : [[contact::P. Culbertson]], Maintenance Manager | ||
: [[contact::G. Davenport]], Compliance Manager | : [[contact::G. Davenport]], Compliance Manager | ||
| Line 559: | Line 584: | ||
==ITEMS OPENED, CLOSED, AND DISCUSSED== | ==ITEMS OPENED, CLOSED, AND DISCUSSED== | ||
===Opened=== | ===Opened=== | ||
None | None | ||
===Opened and Closed=== | ===Opened and Closed=== | ||
: 05000287/2007005-01 | : 05000287/2007005-01 NCV Inadequate Loss of Unit 3 SFP Cooling Procedure (Section 1R20b.(1)) | ||
: 05000287/2007005-02 | : 05000287/2007005-02 NCV Failure to Establish Adequate Procedures for Containment Closure Following a Loss of Decay Heat Removal Event (Section 1R20b.(2)) | ||
===Closed=== | ===Closed=== | ||
: 05000269/2007002-00 | : 05000269/2007002-00 LER Cask Shipments Include Startup Neutron Sources Not Listed in Certificate of Compliance (Section 4OA3) | ||
Items | Items | ||
===Discussed=== | ===Discussed=== | ||
None | None | ||
Latest revision as of 18:20, 14 January 2025
| ML080350435 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 01/31/2008 |
| From: | Moorman J NRC/RGN-II/DRP/RPB1 |
| To: | Baxter D Duke Energy Carolinas, Duke Power Co |
| References | |
| EA-08-037 IR-07-005 | |
| Download: ML080350435 (34) | |
Text
January 31, 2008
SUBJECT:
OCONEE NUCLEAR STATION - INTEGRATED INSPECTION REPORT 05000269/2007005, 05000270/2007005, 05000287/2007005
Dear Mr. Baxter:
On December 31, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Oconee Nuclear Station. The enclosed report documents the inspection findings which were discussed on January 09, 2008, with Mr. M. Glover and other members of your staff.
The inspection examined activities conducted under your licenses as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your licenses. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
This report documents two findings (one self-revealing and one NRC-identified) of very low safety significance (Green) which were determined to be violations of NRC requirements. In addition, two licensee-identified violations are also listed in this report. However, because of their very low safety significance and because they have been entered into your corrective action program, the NRC is treating these violations as non-cited violations (NCVs) in accordance with Section VI.A.1 of the NRCs Enforcement Policy. If you contest any NCV in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the United States Nuclear Regulatory Commission, ATTN:
Document Control Desk, Washington, D.C. 20555-0001, with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at the Oconee facility.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
James H. Moorman, III Chief Reactor Projects Branch 1 Division of Reactor Projects Docket Nos.:
50-269, 50-270, 50-287 License Nos.: DPR-38, DPR-47, DPR-55
Enclosure:
NRC Integrated Inspection Report 05000269/2007005, 05000270/2007005, 05000287/2007005 w/Attachment: Supplemental Information
REGION II==
Docket Nos:
50-269, 50-270, 50-287 License Nos:
DPR-38, DPR-47, DPR-55 Report No:
05000269/2007005, 05000270/2007005, 05000287/2007005 Licensee:
Duke Power Company LLC Facility:
Oconee Nuclear Station, Units 1, 2, and 3 Location:
7800 Rochester Highway Seneca, SC 29672 Dates:
October 1, 2007 - December 31, 2007 Inspectors:
D. Rich, Senior Resident Inspector A. Hutto, Resident Inspector E. Riggs, Resident Inspector A. Vargas-Mendez, Reactor Inspector (Sections 1R08, 4OA7)
M. Coursey, Reactor Inspector (Sections 1R08, 4OA7)
Approved by:
James H. Moorman, III, Chief Reactor Projects Branch 1 Division of Reactor Projects
Enclosure
SUMMARY OF FINDINGS
IR 05000269/2007005, IR 05000270/2007005, IR 05000287/2007005, 10/01/2007 -
12/31/2007; Oconee Nuclear Station, Units 1, 2, and 3; Refueling & Outage Activities.
The report covered a three-month period of inspection by the three onsite resident inspectors and two regional reactor inspectors. Two Green non-cited violations (NCVs)were identified. The significance of most findings is indicated by their color (Green,
White, Yellow, Red) using IMC 0609, "Significance Determination Process" (SDP).
Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.
NRC Identified and Self-Revealing Findings
Cornerstone: Initiating Events
- Green.
A self-revealing non-cited violation (NCV) of Technical Specification (TS)5.4.1 was identified for failure to establish and implement an adequate procedure for loss of the Unit 3 spent fuel pool (SFP) cooling and/or level. More specifically,
Abnormal Procedure AP/3/A/1700/035, Loss of SFP Cooling and/or Level, did not reflect the dependency that Unit 3 SFP cooling has on condenser circulating water (CCW) booster pump flow. If it had, the unexpected Unit 3 SFP temperature increase on December 1, 2007, could have been mitigated in a more timely manner and the SFP temperature increase limited to a lower value.
The licensees failure to adequately establish and implement the procedure for loss of spent fuel pool cooling was a performance deficiency. The finding was considered to be more than minor because it affected the initiating events cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions. The finding was not suitable for SDP evaluation, but was reviewed by NRC management and was determined to be of very low safety significance, because the rate of SFP heatup was low (10 degrees F in four hours), the operators demonstrated the ability to restore CCW booster pump flow within a relatively short time period with respect to the heatup rate, and the Unit 1 and 2 recirculating cooling water (RCW) system was available to be lined up to supply cooling to the Unit 3 SFP cooling heat exchangers per existing plant procedures if needed.
This finding was entered into the licensees corrective action program. It had a cross-cutting aspect of complete, accurate, and up-to-date procedures (H.2.c), as described in the resources component of the human performance cross-cutting area. (Section 1R20b.(1))
Cornerstone: Barrier Integrity
- Green.
The inspectors identified an NCV of TS 5.4.1 for the failure to establish and implement adequate procedures for containment closure following a potential loss of decay heat removal (LDHR) event. More specifically, existing procedures did not adequately address control of vehicles blocking the equipment hatch opening, as was the case on October 31, 2007.
The licensees failure to implement adequate procedures to close the equipment hatch in the event of a LDHR was considered to be a performance deficiency.
The finding was determined to be more than minor as it was associated with the barrier integrity cornerstone attribute of procedure quality, thereby impacting the associated cornerstone objective of providing reasonable assurance that physical design barriers (fuel cladding, reactor coolant system, and containment)protect the public from radionuclide releases caused by accidents or events. The inspectors reviewed this finding in accordance with IMC 0609, Appendix G,
Shutdown Operations Significance Determination Process, Attachment 1,
Checklist 3. This finding did not meet the criteria in the checklist for requiring a Phase 2 or 3 analysis, and was therefore determined to be of very low safety significance.
This finding was entered into the licensees corrective action program. It had a cross-cutting aspect of complete, accurate, and up-to-date procedures (H.2.c), as described in the resources component of the human performance cross-cutting area. (Section 1R20b.(2))
Licensee-Identified Violations
Two violations of very low safety significance, which were identified by the licensee, have been reviewed by the inspectors. Corrective actions taken or planned by the licensee have been entered into the licensees corrective action program. These violations are listed in Section 4OA7.
REPORT DETAILS
Summary of Plant Status:
Unit 1 began the report period at 100 percent rated thermal power (RTP). On October 12, 2007, the unit was reduced to 20 percent RTP to add oil to the 1B1 and 1B2 reactor coolant pumps. The unit was returned to 100 percent RTP on October 13, 2007, where it remained until the end of the inspection period.
Unit 2 began the report period at 100 percent RTP. On November 23, 2007, the unit was reduced to approximately 88 percent RTP for turbine valve movement testing. The unit was returned to 100 percent RTP on November 24, 2007, where it remained until the end of the inspection period.
Unit 3 began the report period at 100 percent RTP. On October 16, 2007, the unit began an end-of-cycle (EOC) coast down until October 26, when it was shutdown from 87 percent RTP for refueling outage EOC 23. On December 16, 2007, Unit 3 was taken critical following outage activities and achieved 100 percent RTP on December 23, 2007, where it remained until the end of the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity
==1R01 Adverse Weather Protection
Cold Weather Preparations
a. Inspection Scope
==
The inspectors reviewed the licensees preparations for adverse weather associated with cold ambient temperatures for the three risk significant systems listed below. This included field walkdowns to assess the material condition and operation of freeze protection equipment (e.g., heat tracing, instrument box heaters, area space heaters, etc.), as well as other preparations made to protect plant equipment from freeze conditions. In addition, the inspectors conducted discussions with operations, engineering, and maintenance personnel responsible for implementing the licensees cold weather protection program to assess the licensees ability to identify and resolve deficient conditions associated with cold weather protection equipment prior to cold weather events. Documents reviewed during this inspection are listed in the Attachment to this report.
- Essential Siphon Vacuum System
- Unit 1, 2 and 3 Borated Water Storage Tank Level Instrumentation
- Elevated Water Storage Tank Level Instrumentation
b. Findings
No findings of significance were identified.
==1R04 Equipment Alignment
==
.1 Partial Walkdown
a. Inspection Scope
The inspectors conducted partial equipment alignment walkdowns to evaluate the operability of selected redundant trains or backup systems while the other train or system was inoperable or out-of-service (OOS). The walkdowns included, as appropriate, reviews of plant procedures and other documents to determine correct system lineups, and verification of critical components to identify any discrepancies which could affect operability of the redundant train or backup system. Documents reviewed are listed in the Attachment to this report. The following three systems were included in this review:
- 3A and 3B Motor Driven Emergency Feedwater pumps with the Unit 3 Turbine Driven Emergency Feedwater (TDEFW) pump OOS for maintenance
- Unit 1/2/3 TDEFW pumps with the Standby Shutdown Facility (SSF) Auxiliary Service Water pump OOS for maintenance
b. Findings
No findings of significance were identified.
.2 Complete Walkdown of the Unit 3 Emergency Feedwater System (EFW)
a. Inspection Scope
The inspectors performed a system walkdown on accessible portions of the Unit 3 EFW system. The inspectors focused on verifying proper valve and breaker positioning, power availability, no damage to piping or cable tray structural supports, and material condition.
A review of Problem Investigation Process reports (PIPs) and open maintenance work orders was performed to verify that material condition deficiencies did not significantly affect the EFW systems ability to perform its design functions and appropriate corrective action was being taken by the licensee.
The inspectors conducted a review of the system engineers trending data and system health reports to verify that appropriate trending parameters were being monitored and that no adverse trends were noted. Documents and drawings reviewed for this semi-annual inspection sample are listed in the Attachment to this report.
b. Findings
No findings of significance were identified.
==1R05 Fire Protection Fire Area Walkdowns
a. Inspection Scope
==
The inspectors conducted tours in eleven areas of the plant to verify that combustibles and ignition sources were properly controlled, and that fire detection and suppression capabilities were intact. The inspectors selected the areas based on a review of the licensees safe shutdown analysis and the probabilistic risk assessment based sensitivity studies for fire-related core damage sequences. Documents reviewed are listed in the Attachment to this report. Inspections of the following areas were conducted during this inspection period:
- Unit 1 and 2 Low Pressure Injection (LPI) Pump Rooms (3)
- Unit 1 and 2 High Pressure Injection (HPI) Pump Rooms (1)
- Unit 1 and 2 Penetration Rooms (4)
- CT-5 Transformer (1)
- Unit 1, 2, and 3 Blockhouses (2)
b. Findings
No findings of significance were identified.
==1R06 Flood Protection Measures (Internal)
a. Inspection Scope
==
The inspectors reviewed the licensees turbine building flood control measures while performing Unit 3 condenser maintenance during its refueling outage commencing in October 2007. The inspectors determined that the licensee complied with the applicable Unit 1 waterbox and condenser circulating water (CCW) inlet and outlet de-watering and watering operating procedures (OP/1/A/1104/012 E and G). The inspectors also walked down the appropriate CCW valve isolations to verify that they were established per Selected Licensee Commitments 16.9.11.
b. Findings
No findings of significance were identified.
==1R08 Inservice Inspection (ISI) Activities
==
.1 Piping Systems ISI
a. Inspection Scope
From November 5-16, 2007, the inspectors reviewed the implementation of the licensees ISI program for monitoring degradation of the reactor coolant system (RCS)boundary and risk significant piping system boundaries. The inspectors reviewed a sample from activities performed during the Unit 3 Fall 2007 refueling outage including non-destructive examinations (NDE) required by the 1998 Edition, 2000 Addenda, of American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel Code,Section XI, and augmented examination commitments.
The inspectors observed and reviewed non-destructive examination (NDE) activities.
Specifically:
Ultrasonic Examination (UT):
- 2B Steam Generator main steam line pipe to nozzle
- 3A Steam Generator nozzle to pipe weld, weld # 3SGA-W3
- 3B Steam Generator reducer to nozzle, weld # 3MS-137-19V
- 3B Steam Generator reducer to nozzle, weld # 3MS-137-22V Liquid Penetrant Testing (LPT):
- High Pressure Injection pipe to flange, weld #s 3HP-252-4A Visual Examination (VT):
- Reactor Vessel (RV) Head Penetrations
- RV Closure Head Control Rod Drive Mechanism Nozzle Penetration Magnetic Particle Testing (MT):
- 2B Steam Generator main steam line pipe to nozzle
- Reactor Coolant System pipe to elbow, weld #3RC-283-8V
- 3A Steam Generator nozzle to pipe weld, weld # 3SGA-W3 Qualification and certification records for examiners, inspection equipment, and consumables along with the applicable NDE procedures for the previously referenced ISI examination activities were reviewed and compared to requirements stated in ASME Section V, ASME Section XI, and other industry standards.
The inspectors reviewed welding activities from the previous outage. The inspectors reviewed drawings, work instructions, weld process sheets, weld travelers, pre-heat requirements and NDE for welding of an ASME Class 1 and 2 pressure boundary weld.
Specific items included:
- LPT: 3B letdown cooler, weld #: 3HP0503-31
- LPT/UT: Low pressure service water piping, weld #: 3LPS-0762-1, 3LPS-076-2 The inspectors reviewed and observed weld overlay and NDE activities associated with the Pressurizer weld overlay activities. Specifically welding and LPT for Pressurizer Safety Relief Valves:
- PZR-WP-91-1
- PZR-WP-91-2
- PZR-WP-91-3
b. Findings
No findings of significance were identified.
.2 Boric Acid Corrosion Control (BACC) Program
a. Inspection Scope
The inspectors reviewed the licensees Boric Acid Corrosion Control (BACC) program to ensure compliance with commitments made in response to NRC Generic Letter 88-05, Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary Components in PWR Plants.
The inspectors conducted an on-site record review, as well as an independent walkdown of parts of the reactor building that are not normally accessible during at-power operations, to evaluate compliance with licensee BACC program requirements and 10CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. In particular, the inspectors assessed whether the visual examinations focused on locations where boric acid leaks can cause degradation of safety-significant components and that degraded or non-conforming conditions were properly identified in the licensees corrective action system.
The inspectors reviewed a sample of engineering evaluations completed for boric acid found on reactor coolant system piping and components to verify that the minimum design code-required section thickness had been maintained for the affected components. The inspectors also reviewed licencee PIPs and corrosion assessments implemented for evidence of boric acid leakage to confirm that they were consistent with requirements.
b. Findings
No findings of significance were identified.
.3 Steam Generator (SG) Tube ISI
a. Inspection Scope
The inspectors reviewed the SG examination scope, expansion criteria, eddy current testing (ET) acquisition procedures, ET analysis procedures, the SG Operational Assessment, in-situ tube pressure testing procedures, and records and examination reports to confirm that:
- The SG tube ET scope was sufficient to identify tube degradation, confirming that the ET scope completed was consistent with the licensees procedures and plant TS requirements. In addition, the inspectors reviewed the SG tube ET scope to determine that it was consistent with that recommended in EPRI Pressurized Water Reactor Steam Generator Examination Guidelines, Revision 6, and included tube areas which represent ET challenges, such as the tube sheet regions, expansion transitions and support plates.
- The ET probes and equipment configurations used to acquire ET data from the SG tubes were qualified to detect the known/expected types of SG tube degradation in accordance with Appendix H, Performance Demonstration for Eddy Current Examination, of EPRI Pressurized Water Reactor Steam Generator Examination Guidelines, Revision 6.
- The licensee adequately evaluated for any contractor deviations from their ET data acquisition or analysis procedures or EPRI Pressurized Water Reactor Steam Generator Examination Guidelines, Revision 6.
b. Findings
No findings of significance were identified.
.4 Identification and Resolution of Problems
a. Inspection Scope
The inspectors performed a review of SG and ISI-related problems that were identified by the licensee and entered into the corrective action program. The inspectors reviewed these corrective action program documents to confirm that the licensee had appropriately described the scope of the problems. In addition, the inspectors review included confirmation that the licensee had an appropriate threshold for identifying issues and had implemented effective corrective actions. The inspectors evaluated the threshold for identifying issues through interviews with licensee staff and review of licensee actions to incorporate lessons learned from industry issues related to the ISI program. The inspectors performed these reviews to ensure compliance with 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Action, requirements.
b. Findings
No findings of significance were identified.
==1R11 Licensed Operator Requalification Simulator Training
a. Inspection Scope
==
The inspectors observed licensed operator simulator training on October 19, 2007. The scenario involved training on emergency operating procedure rules one through five.
This basis for specific actions in each rule was discussed, and the operators proficiency in mitigating associated events was exercised. The inspectors observed crew performance in terms of communications; ability to take timely and proper actions; prioritizing, interpreting, and verifying alarms; correct use and implementation of procedures, including the alarm response procedures; timely control board operation and manipulation, including high-risk operator actions; and oversight and direction provided by the shift supervisor, including the ability to identify and implement appropriate Technical Specification (TS) actions and properly classify the simulated event.
b. Findings
No findings of significance were identified.
==1R12 Maintenance Effectiveness
a. Inspection Scope
==
The inspectors reviewed the licensees effectiveness in performing routine maintenance activities. This review included an assessment of the licensees practices pertaining to the identification, scoping, and handling of degraded equipment conditions, as well as common cause failure evaluations. For each item selected, the inspectors performed a detailed review of the problem history and surrounding circumstances, evaluated the extent of condition reviews as required, and reviewed the generic implications of the equipment and/or work practice problem. For those structures, systems, and components (SSCs) scoped in the maintenance rule, the inspectors verified that reliability and unavailability were properly monitored and that 10 CFR 50.65 (a)(1) and (a)(2) classifications were justified in light of the reviewed degraded equipment condition. The inspectors reviewed the following items:
- PIP O-07-4674, 2A High Pressure Injection Pump Shaft/Seal Overheating Due to Throttle Bushing Contact
b. Findings
No findings of significance were identified.
==1R13 Maintenance Risk Assessment and Emergent Work Evaluations
a. Inspection Scope
==
For the six selected SSCs and activities listed below, the inspectors evaluated the following attributes:
- (1) the effectiveness of the risk assessments performed before maintenance activities were conducted;
- (2) the management of risk;
- (3) that, upon identification of an unforeseen situation, necessary steps were taken to plan and control the resulting emergent work activities; and
- (4) that maintenance risk assessments and emergent work problems were adequately identified and resolved.
- PIP O-07-5669, SSF Unavailable Due to Heating, Ventilation and Cooling Control Timer Failures
- PIP O-07-5705, KHU 1 Governor Oil Pump Operability With Scheduled Yellow Bus Maintenance
- Orange Operational Risk Assessment Management Risk Condition, SSF Monthly PMs During Unit 3 EOC 23 (Auxiliary Building/Turbine Building Flood)
- Critical Action Plan for SSF Monthly Diesel Surveillance During Unit 3 EOC 23
- 230 KV Switchyard Work (PCB-8 PMs) with the Keowee Overhead Path OOS
b. Findings
Inspectors noted one licensee identified violation associated with PIP O-07-5829, which is documented in Section 4OA7 of this report.
==1R15 Operability Evaluations
a. Inspection Scope
==
The inspectors reviewed selected operability evaluations affecting risk significant systems, to assess, as appropriate:
- (1) the technical adequacy of the evaluations;
- (2) whether continued system operability was warranted;
- (3) whether other existing degraded conditions were considered;
- (4) whether identified compensatory measures were in place, would work as intended, and were appropriately controlled; and
- (5) the impact on TS limiting conditions for operation, where continued operability was considered unjustified. Documents reviewed are listed in the Attachment to this report.
The inspectors reviewed the following seven operability evaluations:
- PIP O-07-5593, KHU Governor Control System Critical Alarms
- PIP O-07-5711, Unit 3 Voltage and Load Margin Assessment
- PIP O-07-5786, Foreign Material Found in the 3A LPI Cooler When Opened for Cleaning and Eddy Current Inspection
- PIP O-07-5872, 2B LPI Pump Inboard Bearing Oil Bubbler Emptied Twice During Post-Maintenance Testing Following Lubrication PM
- PIP O-07-6053, Uninterruptible Power Supply Failure
- PIP O-07-6149, Keowee Main Transformer Fan OOS
- PIP O-07-6314, 3PAM MT0080 Was Found Out of Tolerance
b. Findings
No findings of significance were identified.
==1R19 Post-Maintenance Testing (PMT)
a. Inspection Scope
==
The inspectors reviewed PMT procedures and/or test activities, as appropriate, for selected risk significant systems to assess whether:
- (1) the effect of testing on the plant had been adequately addressed by control room and/or engineering personnel;
- (2) testing was adequate for the maintenance performed;
- (3) acceptance criteria were clear and operational readiness was adequately demonstrated consistent with design and licensing basis documents;
- (4) test instrumentation had current calibrations, range, and accuracy consistent with the application;
- (5) tests were performed as written with applicable prerequisites satisfied;
- (6) installed jumpers or lifted leads were properly controlled;
- (7) test equipment was removed following testing; and
- (8) equipment was returned to the status required to perform its safety function. Documents reviewed are listed in the Attachment to this report. The inspectors observed testing and/or reviewed the results of the following five tests:
- PT/2/A/0203/006A, 2B Low Pressure Injection Pump Test - Recirculation Following Mechanical Seal Cleaning and Pump Lubrication
- PT/3/A/0600/012, Unit 3 TDEFW Pump Test Following the Addition of Stiffeners to the Turbine Support Frame (OD301925)
- PT/1/A/0230/015, High Pressure Injection Motor Cooler Flow Test Following the Relocation of the Low Pressure Service Water (LPSW) Emergency Supply Cuno Filter (OD101743)
- PT/1/A/0251/001, Low Pressure Service Water Pump Test Following a Repack of the Unit 1/2 A Pump
- PT/3/A/0610/028, Main Feeder Bus Lockout Relay Test Following Relay 62BXS23 Replacement
b. Findings
No findings of significance were identified.
==1R20 Refueling & Outage Activities
a. Inspection Scope
==
The inspectors conducted reviews and observations for selected outage activities to ensure that:
- (1) the licensee considered risk in developing the outage plan;
- (2) the licensee adhered to the outage plan to control plant configuration based on risk;
- (3) that mitigation strategies were in place for losses of key safety functions; and
- (4) the licensee adhered to operating license and TS requirements. Between October 27, 2007, and December 22, 2007, the following activities related to the Unit 3 EOC 23 refueling outage were reviewed for conformance to applicable procedures and selected activities associated with each evaluation were witnessed:
- outage risk management plan/assessment
- clearance activities
- reactor coolant system instrumentation
- plant cooldown
- mode changes from Mode 1 (power operation) to No Mode (defueled)
- shutdown decay heat removal and inventory control
- containment closure
- refueling activities
- plant heatup/mode changes
- core physics testing
- power escalation Additionally, in response to operational experience concerns regarding reactor vessel (RV) head lifts (NRC Operating Experience Smart Sample FY2007-03), the inspectors reviewed licensee programs and procedures to determine whether current practices were within the current licensing basis. The inspectors reviewed licensee programs relating to Generic Letter 80-113, Control of Heavy Loads, and NUREG 0612, Control of Heavy Loads at Nuclear Power Plants, and interviewed licensee personnel.
b. Findings
- (1) Inadequate Loss of Spent Fuel Pool Cooling Abnormal Procedure
Introduction:
A Green self-revealing NCV of TS 5.4.1 was identified for failure to establish and implement an adequate procedure for loss of the Unit 3 spent fuel pool (SFP) cooling and/or level.
Description:
On December 1, 2007, Unit 3 was in no mode with the core off-loaded to the Unit 3 SFP when a degraded flow condition occurred in the CCW booster pump flow to the recirculating cooling water (RCW) heat exchangers. This in turn had an effect on SFP cooling, since RCW removes heat from the SFP cooling heat exchangers. The degraded flow was a result of air entrainment by the Unit 3 CCW booster pumps when the Unit 3 CCW header was refilled at approximately 1300 hours0.015 days <br />0.361 hours <br />0.00215 weeks <br />4.9465e-4 months <br />. There were no CCW booster pump flow alarms available to the operators in the control room; therefore, this condition was not initially recognized. At approximately 3:00 pm, the Unit 3 operator at the controls noted that the SFP temperature had increased from 96 degrees F to 99 degrees F. SFP temperature continued to increase to 103 degrees F by 4:00 pm.
During the time of the SFP temperature increase, the operators reviewed AP/3/A/1700/035, Loss of SFP Cooling and/or Level, but never entered the procedure, even though one of the entry conditions was an unexpected increase in SFP temperature. Additionally, the AP does not provide instructions to check CCW booster pump flow, even though this flow is the ultimate heat sink for spent fuel decay heat.
At 4:00 pm, control room operators checked CCW booster pump flows and determined that the flow was degraded (approximately 300 gpm verses an expected 2500 gpm).
The operators correlated the restoration alignment to the SFP temperature increase and operators were dispatched to stop and vent the CCW booster pumps one at a time, as well as the pump suction strainer. This action re-established adequate CCW booster pump flow to the RCW coolers and the SFP temperature eventually decreased to its original value. The maximum SFP temperature resulting from this event was approximately 106 degrees F, for a 10 degree F increase over a four hour period. Had the operators complied with the entry conditions of AP/3/A/1700/035 and entered the AP when the unexpected SFP temperature was recognized, and had the procedure contained instructions to check CCW booster pump flow to RCW, the condition could have been mitigated in a more timely manner and the SFP temperature increase limited to a lower value. Without adequate procedural guidance, the operators relied on plant knowledge to diagnose the reduced CCW booster pump flow.
Analysis:
The inspectors determined that the licensees failure to adequately establish and implement the procedure for loss of spent fuel cooling was a performance deficiency. The finding was considered to be more than minor because it affected the initiating events cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions. The finding was not suitable for SDP evaluation, but was reviewed by NRC management and was determined to be a finding of very low safety significance (Green), because the rate of SFP heatup was low (10 degrees F in four hours), the operators demonstrated the ability to restore CCW booster pump flow within a relatively short time period with respect to the heatup rate, and the Unit 1 and 2 RCW system was available to be lined up to supply cooling to the Unit 3 SFP cooling heat exchangers per existing plant procedures if needed. This finding had a cross-cutting aspect of complete, accurate, and up-to-date procedures (H.2.c), as described in the resources component of the human performance cross-cutting area.
Enforcement:
TS 5.4.1 requires that procedures shall be established, implemented and maintained covering the applicable procedures recommended in Regulatory Guide 1.33.
Regulatory Guide 1.33, Appendix A, Section 5, requires procedures for abnormal, off normal, or alarm conditions. Contrary to the above, the licensee failed to adequately establish and implement the abnormal operating procedure for loss of spent fuel cooling.
Because the finding was determined to be of very low safety significance and has been entered into the licensees corrective action program as PIP O-07-7069, this violation is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
NCV 05000287/2007005-01, Inadequate Loss of Unit 3 SFP Cooling Procedure.
- (2) Inadequate Containment Closure Procedures
Introduction:
The inspectors identified a Green NCV of TS 5.4.1 for the failure to establish and implement adequate procedures for containment closure following a potential loss of decay heat removal (LDHR) event.
Description:
On October 27, 2007, Unit 3 was shutdown for a planned refueling outage.
On October 31, 2007, with the unit in Mode 5, the equipment hatch open, the reactor coolant system vented, and a core-boil time of 23.3 minutes, the inspectors identified a tractor-trailer rig parked in the equipment hatch opening. The rig was unattended and was blocking the equipment hatch and missile shield doors. Security personnel at the hatch and maintenance personnel stationed to close the hatch in an emergency were not aware of the location of the tractor operators or the keys. The licensee subsequently found that the vehicle operators were at another location on the plant site.
Site Directive 1.3.5, Shutdown Protection Plan, required that with a core-boil time of less than 30 minutes, designated maintenance personnel must be pre-positioned outside of the equipment hatch for immediate initiation of hatch closure activities per AM/0/A/1400/002B (Equipment Hatch - Reactor Building - Emergency Closing) in the event of a loss of decay heat removal. The inspectors noted these personnel were stationed as required, but that procedures did not address control of vehicles blocking the hatch opening. The Shutdown Protection Plan provided a time requirement to achieve containment closure based on time to core boil and habitability time. The required closure time on October 31 was 53.3 minutes. When interviewed, maintenance personnel stated if necessary, they would remove the vehicle with the crane provided to handle the equipment hatch. This plan was somewhat re-enforced by prerequisite 6.8 of procedure AM/0/A/1400/002B, which stated, Use mobile crane to clear hatch area. In an emergency, this may have been a success path. However, no specific procedures, rigging, or training had been provided for this purpose. With a large, unattended vehicle blocking the equipment hatch, there was less than adequate assurance that maintenance personnel could remove the vehicle and shut the equipment hatch within the required time.
The licensee estimated that the average containment temperature would reach 110 degrees F approximately 68.3 minutes after a loss of decay heat removal, assuming loss of all containment cooling. The inspectors acknowledged that 68 minutes was a reasonable estimate of the time required to remove the vehicle and shut the equipment hatch. The inspectors also noted additional margin was available, as temperatures at the hatch would be lower than average building temperature, the required tasks could be completed at temperatures above 110 degrees F, and core uncovery and damage would not occur until several hours into the event.
As immediate corrective action, the licensee improved pre-shift briefings of personnel designated to control containment openings, including temporary measures to control obstructions at containment openings.
Analysis:
The licensees failure to implement adequate procedures to close the equipment hatch in the event of a LDHR was considered to be a performance deficiency.
The finding was determined to be more than minor as it is associated with the barrier integrity cornerstone attribute of procedure quality; thereby, impacting the associated cornerstone objective of providing reasonable assurance that physical design barriers (fuel cladding, reactor coolant system, and containment) protect the public from radionuclide releases caused by accidents or events. The inspectors reviewed this finding in accordance with IMC 0609, Appendix G, Shutdown Operations Significance Determination Process, Attachment 1, Checklist 3. This finding did not meet the criteria in the checklist for requiring a phase 2 or 3 analysis, and was therefore determined to be of very low safety significance (Green). This finding had a cross-cutting aspect of complete, accurate, and up-to-date procedures (H.2.c), as described in the resources component of the human performance cross-cutting area.
Enforcement:
TS 5.4.1 requires that written procedures shall be established, implemented, and maintained covering activities related to procedures recommended in Regulatory Guide 1.33, Rev. 2, Appendix A, 1978. Regulatory Guide 1.33 requires procedures for maintaining containment integrity. Contrary to the above, the licensee failed to implement adequate procedures to establish and maintain containment closure during a potential loss of decay heat removal event. The established procedures failed to provide control of obstructions in the equipment hatch, such that obstructions could be rapidly removed during an event. Because this violation is of low safety significance and has been entered into the licensees corrective action program as PIP O-07-6083, it is being treated as a NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy:
NCV 05000287/2007005-02, Failure to Establish Adequate Procedures for Containment Closure Following a Loss of Decay Heat Removal Event.
- (3) Review of Heavy Lift Practices The inspectors identified the following issues:
- The licensee could not demonstrate that the Updated Final Safety Analysis Report (UFSAR) had been adequately updated to reflect information and analyses provided to the NRC in response to generic communications regarding heavy loads.
- The licensee could not demonstrate that their RV head lifts, which lift the head to approximately 7 feet above the reactor vessel flange, were bounded by any design calculations which evaluated the drop of the head through air onto the RV, upper internals, and irradiated fuel.
- The licensee could not demonstrate that their procedures for the RV head removal and installation ever limited their head lifts to the bounds contained in an June 22, 1982, letter sent to the NRC concerning a load drop analysis for RV head lifts.
Failure to update the Final Safety Analysis Report pursuant to 10 CFR 50.71(e) to reflect aspects of handling the RV head was considered a potential violation.
The NRC has found industry uncertainty regarding the licensing bases for handling of RV heads, and as a result issued EGM 07-006, Enforcement Discretion for Heavy Load Handling Activities, on September 28, 2007. By letter dated September 14, 2007, (ML072670127), the Nuclear Energy Institute (NEI) has informed the NRC of industry approval of a formal initiative that specifies actions each plant will take to ensure that heavy load lifts continue to be conducted safely and that plant licensing bases accurately reflect plant practices. The NRC staff believes implementation of the initiative will resolve uncertainty in the licensing bases for heavy load handling, and enforcement discretion related to the uncertain aspects of the licensing basis is appropriate during the implementation of the initiative.
The inspectors determined that the licensee met the following criteria to warrant enforcement discretion:
1. For RV head lifts occurring during and after April, 2007, the licensee
implemented load handling procedures consistent with the existing load drop analysis.
2. Inspections of the following areas revealed no findings of significance:
- (a) Licensee implementation of safe load paths, load handling procedures, and standards for training of crane operators, use of special lifting devices, use of slings, and design, inspection, testing, and maintenance of the reactor building crane.
- (b) For spent fuel cask lifts over the spent fuel pool, a load drop analysis was provided that bounds the planned lifts with respect to load weight, load height, and medium present under the load. Procedures for handling the load reflected the applicable safety basis.
- (c) The movement of heavy loads was included as a configuration management activity in administrative controls established to implement 10 CFR50.65(a)(4).
Therefore, consistent with the intent of EGM 07-006, the NRC is exercising enforcement discretion (EA-08-037) for the above violation in accordance with Section VII.B.6 of the NRC Enforcement Policy without any enforcement action.
==1R22 Surveillance Testing
a. Inspection Scope
==
The inspectors witnessed surveillance tests and/or reviewed test data of the five risk-significant SSCs listed below, to assess, as appropriate, whether the SSCs met TS, the UFSAR, and licensee procedure requirements. In addition, the inspectors determined if the testing effectively demonstrated that the SSCs were ready and capable of performing their intended safety functions. Documents reviewed are listed in the to this report.
- PT/0/A/0251/010, Auxiliary Service Water Pump Test (IST)
- PT/0/A/0711/001, Zero Power Physics Test (Unit 3)
- PT/3/A/0151/019, Penetration 19 Leak Rate Test (CIV)
b. Findings
No findings of significance were identified.
==1R23 Temporary Plant Modifications
a. Inspection Scope
==
The inspectors reviewed documents and observed portions of the installation of two selected temporary modifications. Among the documents reviewed were system design bases, the UFSAR, TS, system operability/availability evaluations, and the 10 CFR 50.59 screening. As appropriate, the inspectors determined if: the installation was consistent with the modification documents; it was in accordance with the configuration control process; adequate procedures and changes were made; and post installation testing was adequate. The following items were reviewed under this inspection procedure:
- OD 101602, Install Jumpers in Unit 1 Main Transformer Control Cabinet to Bypass Switch 43C (Cooler Selector Switch)
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES
4OA1 Performance Indicator (PI) Verification
a. Inspection Scope
The inspectors verified the Mitigating Systems Performance Indicators (MSPI) listed in the table below (for all three units), to determine its accuracy and completeness against requirements in NEI 99-02, Regulatory Assessment Performance Indicator Guideline.
Cornerstone: Mitigating Systems
Performance Indicator Verification Period Records Reviewed MSPI
- high pressure injection
- emergency feedwater
- emergency AC power
- support cooling water 4th quarter, 2006; 1st, 2nd, and 3rd quarter, 2007
- Operating Logs, Train Unavailability Data
- Maintenance Records
- Maintenance Rule Data
- Corrective Action Program
- Consolidated Data Entry Derivation Reports
- System Health Reports
b. Findings
No findings of significance were identified.
4OA2 Identification and Resolution of Problems
.1 Daily Screening of Corrective Action Reports
As required by Inspection Procedure (IP) 71152, "Identification and Resolution of Problems, and in order to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed daily screening of items entered into the licensees corrective action program. This screening was accomplished by reviewing copies of PIPs, attending daily screening meetings, and accessing the licensees computerized database.
.2 Semi-Annual Trend Review
a. Inspection Scope
As required by IP 71152, "Identification and Resolution of Problems," the inspectors performed a review of the licensees Corrective Action Program (CAP) and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screenings discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six month period of July 2007 through December 2007, although some examples expanded beyond those dates when the scope of the trend warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, plant health team vulnerability lists, focus area reports, system health reports, self-assessment reports, maintenance rule reports, and Safety Review Group Monthly Reports. The inspectors compared and contrasted their results with the results contained in the licensees latest quarterly trend reports.
Corrective actions associated with a sample of the issues identified in the licensees trend report were reviewed for adequacy.
b.
Assessment and Observations No findings of significance were identified. In general, the licensee has identified trends and has appropriately addressed the trends with their CAP.
.3 Focused Review
a. Inspection Scope
The inspectors performed an in-depth review of one issue entered into the licensees CAP, and also performed an in-depth review of existing plant operator workarounds.
The samples were within the Mitigating Systems Cornerstone and involved risk significant systems. The inspectors reviewed the actions taken to determine if the licensee had adequately addressed the following attributes:
- Complete, accurate and timely identification of the problem
- Evaluation and disposition of operability and reportability issues
- Consideration of previous failures, extent of condition, generic or common cause implications
- Prioritization and resolution of the issue commensurate with safety significance
- Identification of the root cause and contributing causes of the problem
- Identification and implementation of corrective actions commensurate with the safety significance of the issue.
The following issues and corrective actions were reviewed:
- Operator Workarounds
- PIP 07-3982, SSF Auxiliary Service Water (ASW) Suction Pipe Air Ejector Performance Has Degraded
b. Findings
No findings of significance were identified.
4OA3 Event Followup
(Closed) Licensee Event Report (LER) 05000269/2007002-00, Cask Shipments Include Startup Neutron Sources Not Listed in Certificate of Compliance (COC). This issue concerned a shipment of spent fuel from Oconee to McGuire in 1987 which included two startup neutron sources. Shipping fuel assemblies with a startup source violated shipping cask COC Number 9015, Revision 13. The issue was identified by the licensee and adequately addressed in the corrective action program under PIPs M-07-5072, O-06-4569, and G-95-0896. This failure to comply with the COC constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section IV of the NRC's Enforcement Policy. This LER is closed.
4OA6 Management Meetings (Including Exit Meeting)
.1
Exit Meeting Summary
The inspectors presented the inspection results to Mr. M. Glover, Oconee Station Manager, and other members of licensee management at the conclusion of the inspection on January 9, 2008. The licensee acknowledged the findings presented. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary. No proprietary information was identified.
.2 Regulatory Performance Meeting
A public Regulatory Performance Meeting was held on December 5, 2007, at the Oconee World of Energy Visitor Center. The purpose of this meeting was to discuss the performance deficiencies, lessons learned, and the proposed corrective actions associated with the two White findings and the White performance indicator in the Mitigating Systems Cornerstone that resulted in the performance of all three Oconee Units being in the Degraded Cornerstone Column of the NRCs Action Matrix from the fourth quarter 2006 to the third quarter 2007. The required supplemental inspection of these three White issues was completed on August 31, 2007, and the results were reported in NRC Supplemental Inspection Report 05000269,270,287/2007009, dated October 12, 2007. Meeting attendees are listed in the Attachment below.
4OA7 Licensee Identified Violations
The following violations of very low safety significance (Green) were identified by the licensee and are violations of NRC requirements which meet the criteria of Section VI of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a NCVs.
- 10 CFR Part 50.65 (a)(4), requires, in part, that prior to performing maintenance activities, the licensee assess the potential risk increase resulting from the proposed maintenance activities. Contrary to the above, on October 21, 2007, the licensee failed to adequately assess the risk associated with activities to pressurize the Unit 3 Reactor Building (RB) while the 3A LPI cooler was OOS for maintenance. On October 22, 2007, the licensee identified and corrected the inadequate risk assessment, which changed the units risk profile from Yellow to Orange. The licensee halted activities to pressurize the U3 RB, which returned the units risk profile to Yellow. In accordance with Inspection Manual Chapter (IMC) 0612 Appendix B, Issue Screening and Appendix E, Examples of Minor Issues, Section 7. Maintenance Rule Issues, Example e., the issue was determined to be more than minor. This finding is of very low safety significance because the incremental core damage probability was determined to be zero, and the incremental large early release probability was determined to be less than 1.2 E-9. This finding was documented in the licensees corrective action program as PIP O-07-5829.
- 10 CFR 50.55a(g)(4) requires, in part, that components classified as ASME Code Class III must meet the requirements set forth in Section XI of the ASME Code.
The 1998 Edition of Section XI, Article IWA-5244, Buried Components, requires that in non-redundant systems where the buried components are isolable by means of valves, the visual examination for leakage (VT-2) shall consist of a leakage test that determines the rate of pressure loss. Alternatively, the test may determine the change in flow between the ends of the buried components.
Contrary to the above, the licensee had not met these requirements during their third ISI interval which ended in 2005. The licensee recently identified this issue in their corrective action program as PIP O-07-06007. The licensee generated corrective actions to identify all code class buried piping and update the ISI program in order to support testing of the affected piping. This finding is of very low safety significance because it was not a design or qualification deficiency resulting in a loss of operability, did not represent an actual loss of a safety function, did not result in exceeding a TS allowed outage time, and did not affect external event mitigation.
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- E. Anderson, Superintendent of Operations
- S. Batson, Engineering Manager
- D. Baxter, Site Vice President
- R. Brown, Emergency Preparedness Manager
- E. Burchfield, Reactor and Electrical Systems Manager
- S. Capps, Mechanical and Civil Engineering Manager
- N. Constance, Operations Training Manager
- C. Curry, Mechanical/Civil Engineering Manager
- P. Culbertson, Maintenance Manager
- G. Davenport, Compliance Manager
- R. Freudenberger, Safety Assurance Manager
- M. Glover, Station Manager
- C. Gray, Regulatory Compliance
- D. Hubbard, Training Manager
- T. King, Security Manager
- B. Meixell, Regulatory Compliance
- J. Smith, Regulatory Affairs
- J. Steeley, Training Supervisor
- S. Severance, Regulatory Compliance
- J. Twiggs, Radiation Protection Manager
- J. Weast, Regulatory Compliance
NRC
- J. Moorman, III, Chief, Reactor Projects Branch 1, RII
- C. Casto, Acting Deputy Regional Administrator, RII
- D. Rich, Senior Resident Inspector
- K. Clark, Senior Public Affairs Officer
Other
- G. Brouette, HSBCT, Site ANII
- T. Clements, Nuclear Watch South
- R. Chandler, Anderson Independent
- A. Simon, Greenville News
- D. Mangrum, WGOG/WSNW
- Note: asterisk (*) reflects attendance at Regulatory Performance Meeting on December 5, 2007
ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
None
Opened and Closed
- 05000287/2007005-01 NCV Inadequate Loss of Unit 3 SFP Cooling Procedure (Section 1R20b.(1))
- 05000287/2007005-02 NCV Failure to Establish Adequate Procedures for Containment Closure Following a Loss of Decay Heat Removal Event (Section 1R20b.(2))
Closed
- 05000269/2007002-00 LER Cask Shipments Include Startup Neutron Sources Not Listed in Certificate of Compliance (Section 4OA3)
Items
Discussed
None