IR 05000373/2008004: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(StriderTol Bot change)
 
(6 intermediate revisions by the same user not shown)
Line 1: Line 1:
{{Adams|number = ML083100251}}
{{Adams
| number = ML083100251
| issue date = 11/04/2008
| title = IR 05000373-08-004, 05000374-08-004; Exelon Generation Company, LLC; 7/01/2008 - 9/30/2008; LaSalle County Station, Units 1 & 2, Routine Integrated Report
| author name = Riemer K
| author affiliation = NRC/RGN-III/DRP/B2
| addressee name = Pardee C
| addressee affiliation = AmerGen Energy Co, LLC, Exelon Nuclear
| docket = 05000373, 05000374
| license number = NPF-011, NPF-018
| contact person =
| document report number = IR-08-004
| document type = Inspection Report, Letter
| page count = 46
}}


{{IR-Nav| site = 05000373 | year = 2008 | report number = 004 }}
{{IR-Nav| site = 05000373 | year = 2008 | report number = 004 }}


=Text=
=Text=
{{#Wiki_filter:
{{#Wiki_filter:November 4, 2008
[[Issue date::November 4, 2008]]


Mr. Charles President and Chief Nuclear Officer (CNO), Exelon Nuclear Chief Nuclear Officer (CNO), AmerGen Energy Company, LLC 4300 Winfield Road Warrenville IL 60555
==SUBJECT:==
LASALLE COUNTY STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000373/2008004; 05000374/2008004


SUBJECT: LASALLE COUNTY STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000373/2008004; 05000374/2008004
==Dear Mr. Pardee:==
On September 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your LaSalle County Station, Units 1 and 2. The enclosed report documents the results of this inspection, which were discussed on October 2, 2008, with Site Vice President, Mr. Daniel Enright, and other members of your staff.
 
The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
 
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
 
Based on the results of this inspection, no NRC-identified or self-revealed findings of safety significance were identified. There were no findings involving a violation of NRC requirements.
 
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Sincerely,
/RA/
 
Kenneth Riemer, Chief Branch 2 Division of Reactor Projects Docket Nos. 50-373; 50-374 License Nos. NPF-11; NPF-18
 
Enclosure:
Inspection Report 05000373/2008004; 05000374/2008004 w/Attachment: Supplemental Information cc w/encl:
Site Vice President - LaSalle County Station
 
Plant Manager - LaSalle County Station
 
Regulatory Assurance Manager - LaSalle County Station
 
Chief Operating Officer and Senior Vice President
 
Senior Vice President - Midwest Operations
 
Senior Vice President - Operations Support
 
Vice President - Licensing and Regulatory Affairs
 
Director - Licensing and Regulatory Affairs


==Dear Mr. Pardee:==
Manager Licensing - Braidwood, Byron and LaSalle
On September 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your LaSalle County Station, Units 1 and 2. The enclosed report documents the results of this inspection, which were discussed on October 2, 2008, with Site Vice President, Mr. Daniel Enright, and other members of your staff. The inspection examined activities conducted under your license as they relate to safety and compliance with the Commission's rules and regulations and with the conditions of your license. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no NRC-identified or self-revealed findings of safety significance were identified. There were no findings involving a violation of NRC requirements. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
Associate General Counsel


Sincerely,/RA/ Kenneth Riemer, Chief Branch 2 Division of Reactor Projects Docket Nos. 50-373; 50-374 License Nos. NPF-11; NPF-18
Document Control Desk - Licensing


===Enclosure:===
Assistant Attorney General J. Klinger, State Liaison Officer, Illinois Emergency Management Agency
Inspection Report 05000373/2008004; 05000374/2008004


===w/Attachment:===
Chairman, Illinois Commerce Commission
Supplemental Information cc w/encl: Site Vice President - LaSalle County Station Plant Manager - LaSalle County Station Regulatory Assurance Manager - LaSalle County Station Chief Operating Officer and Senior Vice President Senior Vice President - Midwest Operations Senior Vice President - Operations Support Vice President - Licensing and Regulatory Affairs Director - Licensing and Regulatory Affairs Manager Licensing - Braidwood, Byron and LaSalle Associate General Counsel Document Control Desk - Licensing Assistant Attorney General J. Klinger, State Liaison Officer, Illinois Emergency Management Agency Chairman, Illinois Commerce Commission


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
.........................................................................................................1
IR 05000373/2008004, 05000374/2008004; 7/01/2008 - 9/30/2008; LaSalle County Station,
 
Units 1 & 2; routine integrated report.
 
The inspection was conducted by U.S. Nuclear Regulatory Commission (NRC) resident inspectors and regional inspectors. The report covers a three-month period of resident inspection, and announced inspection in the areas of health physics, heat sink performance, and diesel generator performance testing. No findings of significance were identified. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.
 
Inspector-Identified and Self-Revealed Findings No findings of significance were identified.
 
===Licensee-Identified Violations===
No violations of significance were identified.


=REPORT DETAILS=
=REPORT DETAILS=
.....................................................................................................................2 Summary of Plant Status.........................................................................................................2
 
===Summary of Plant Status===
Unit 1 The unit began the inspection period operating at full power. On July 20, 2008, the unit was reduced to 82 percent for motor driven reactor feed pump and main turbine valve surveillance testing. The unit returned to full power that same day. On September 6, 2008, power was reduced to approximately 66 percent to perform control rod sequence exchange and scram time testing. Operation at full power resumed on September 7, 2008. On September 28, 2008, the unit was shutdown to perform repairs of a hydrogen leak on the main generator housing. The unit remained in mode 3 (hot shutdown) for the rest of the inspection period.
 
Unit 2 The unit began the inspection period operating at full power. On July 27, 2008, power was reduced to approximately 62 percent for channel distortion testing of all the interior rods. The unit was returned to full power that same day. On August 30, 2008, the unit commenced a reduction in power to 53 percent for control rod sequence exchange and feedwater pump turbine surveillances. The unit was returned to full power on August 31, 2008, where it remained until September 26, 2008. At this time, power was reduced to 55 percent for power suppression testing, control rod SCRAM time testing and channel distortion testing. Full power was restored on September 29, 2008, and the unit remained operating at or near full power for the rest of the inspection period.


==REACTOR SAFETY==
==REACTOR SAFETY==
..................................................................................2
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness
{{a|1R04}}
{{a|1R04}}
==1R04 Equipment Alignment==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
{{IP sample|IP=IP 71111.04}}
...............................................................2
 
{{a|1R05}}
===.1 Quarterly Partial System Walkdowns===
====a. Inspection Scope====
The inspectors performed partial system walkdowns of the following risk-significant systems:
* Unit 2 low pressure core spray (LPCS);
* 2A standby liquid control (SLC) with 2B out-of-service; and
* 1A and 2A diesel generators (DG) and support systems with the 0 DG out of service.
 
The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program (CAP) with the appropriate significance characterization. Documents reviewed are listed in the Attachment.
 
These activities constituted three partial system walkdown samples as defined in Inspection Procedure (IP) 71111.04-05.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Semi-Annual Complete System Walkdown===
====a. Inspection Scope====
On August 27 through August 29, 2008, the inspectors performed a complete system alignment inspection of the fire protection system to verify the functional capability of the system. This system was selected because it was considered risk-significant in the licensees probabilistic risk assessment. The inspectors walked down the system to review mechanical and electrical equipment line ups, electrical power availability, system pressure and temperature indications, as appropriate, component labeling, component lubrication, component and equipment cooling, hangers and supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation. A review of a sample of past and outstanding work orders (WOs)was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the CAP database to ensure that system equipment alignment problems were being identified and appropriately resolved.
 
Documents reviewed are listed in the Attachment to this report.
 
These activities constituted one complete system walkdown sample as defined in IP 71111.04-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R05}}
 
==1R05 Fire Protection==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
{{IP sample|IP=IP 71111.05}}
.........................................................................4
 
{{a|1R07}}
===.1 Routine Resident Inspector Tours===
{{IP sample|IP=IP 71111.05Q}}
 
====a. Inspection Scope====
The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:
* Fire Zone 7B3 0 DG Room;
* Fire Zone 4F2 Unit 2 Division 1 switchgear;
* Fire Zone 2G Unit 1 reactor building 710;
* Fire Zone 214 Unit 1 reactor core isolation cooling (RCIC)/LPCS; and
* Fire Zone 2B1 Unit 1 reactor building 820.
 
The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan.
 
The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP. Documents reviewed are listed in the Attachment to this report.
 
These activities constituted five quarterly fire protection inspection samples as defined in IP 71111.05-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R07}}
 
==1R07 Heat Sink Performance==
==1R07 Heat Sink Performance==
{{IP sample|IP=IP 71111.07T}}
{{IP sample|IP=IP 71111.07T}}
..........................................................4
 
{{a|1R11}}
===.1 Triennial Review of Heat Sink Performance===
====a. Inspection Scope====
The inspectors reviewed operability determinations, completed surveillances, vendor manual information, associated calculations, performance test results and cooler inspection results associated with the 2B Residual Heat Removal (RHR) heat exchanger and the DG common to both units (0 DG) heat exchanger. These heat exchangers were chosen based on their risk significance in the licensees probabilistic safety analysis, their important safety-related mitigating system support functions and their relatively low margin.
 
For the 2B RHR and the 0 DG heat exchangers, the inspectors verified that testing, inspection, maintenance, and monitoring of biotic fouling and macrofouling programs were adequate to ensure proper heat transfer. This was accomplished by verifying the test method used was consistent with accepted industry practices, or equivalent, the test conditions were consistent with the selected methodology, the test acceptance criteria were consistent with the design basis values, and results of heat exchanger performance testing. The inspectors also verified that the test results appropriately considered differences between testing conditions and design conditions, the frequency of testing based on trending of test results was sufficient to detect degradation prior to loss of heat removal capabilities below design basis values and test results considered test instrument inaccuracies and differences.
 
For the 2B RHR and the 0 DG heat exchanger, the inspectors reviewed the methods and results of heat exchanger performance inspections. The inspectors verified the methods used to inspect and clean heat exchangers were consistent with as-found conditions identified and expected degradation trends and industry standards, the licensees inspection and cleaning activities had established acceptance criteria consistent with industry standards, and the as-found results were recorded, evaluated, and appropriately dispositioned such that the as-left condition was acceptable.
 
The inspectors verified the performance of the ultimate heat sink (UHS) and their subcomponents, including piping, intake screens, pumps, and valves, by tests or visual inspection to ensure availability and accessibility to the in-plant cooling water systems.
 
The inspectors reviewed the results of the licensees inspection of the UHS weirs or excavations. The inspectors verified that identified settlement or movement indicating loss of structural integrity and/or capacity was appropriately evaluated and dispositioned by the licensee. In addition, the inspectors verified the licensee ensured sufficient reservoir capacity by trending and removing debris or sediment buildup in the UHS.
 
The inspectors performed a system walkdown of the service water intake structure to verify the licensees assessment on structural integrity and component functionality.
 
This included the verification that licensee ensured proper functioning of traveling screens and strainers, and structural integrity of component mounts. In addition, the inspectors verified that service water pump bay silt accumulation is monitored, trended, and maintained at an acceptable level by the licensee, and that water level instruments are functional and routinely monitored. The inspectors also verified the licensees ability to ensure functionality during adverse weather conditions.
 
In addition, the inspectors reviewed condition reports related to the heat exchangers/coolers and heat sink performance issues to verify that the licensee had an appropriate threshold for identifying issues and to evaluate the effectiveness of the corrective actions. The documents reviewed are included in the Attachment to this report.
 
These inspection activities constituted two heat sink inspection samples as defined in IP 71111.07-05.
 
====b. Findings====
No findings of significance were identified {{a|1R11}}
 
==1R11 Licensed Operator Requalification Program==
==1R11 Licensed Operator Requalification Program==
{{IP sample|IP=IP 71111.11}}
{{IP sample|IP=IP 71111.11}}
.............................6
 
{{a|1R12}}
===.1 Resident Inspector Quarterly Review===
{{IP sample|IP=IP 71111.11Q}}
 
====a. Inspection Scope====
On September 16, 2008, the inspectors observed a crew of licensed operators in the plants simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:
* licensed operator performance;
* crews clarity and formality of communications;
* ability to take timely actions in the conservative direction;
* prioritization, interpretation, and verification of annunciator alarms;
* correct use and implementation of abnormal and emergency procedures;
* control board manipulations;
* oversight and direction from supervisors; and
* ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.
 
The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one quarterly licensed operator requalification program sample as defined in IP 71111.11.
 
====b. Findings====
No findings of significance were identified. {{a|1R12}}
 
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
{{IP sample|IP=IP 71111.12}}
......................................................6
 
{{a|1R13}}
===.1 Routine Quarterly Evaluations===
{{IP sample|IP=IP 71111.12Q}}
 
====a. Inspection Scope====
The inspectors evaluated degraded performance issues involving the following risk significant systems/components:
* Circulating water system; and
* Maintenance rule functional failure assessment for control rod drive (CRD)pressure control bypass valve 1C11-F004.
 
The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensees actions to address system performance or condition problems in terms of the following:
* implementing appropriate work practices;
* identifying and addressing common cause failures;
* scoping of systems in accordance with the Code of Federal Regulations (CFR)10 CFR 50.65(b) of the maintenance rule;
* characterizing system reliability issues for performance;
* charging unavailability for performance;
* trending key parameters for condition monitoring;
* ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and
* verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1).
 
The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted two quarterly maintenance effectiveness samples as defined in IP 71111.12-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
{{IP sample|IP=IP 71111.13}}
..7
 
{{a|1R15}}
===.1 Maintenance Risk Assessments and Emergent Work Control===
====a. Inspection Scope====
The inspectors reviewed the licensees evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:
* Unit 1 motor-driven reactor feed pump protected pathway;
* Unit 2 electro-hydraulic control (EHC) filter emergent replacement;
* 2B non-essential service water jockey pump suction pipe thru-wall flaw; and
* 1B DG protected pathway.
 
These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensees probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.
 
These maintenance risk assessments and emergent work control activities constituted four samples as defined in IP 71111.13-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R15}}
 
==1R15 Operability Evaluations==
==1R15 Operability Evaluations==
{{IP sample|IP=IP 71111.15}}
{{IP sample|IP=IP 71111.15}}
............................................................8
 
{{a|1R18}}
===.1 Operability Evaluations===
====a. Inspection Scope====
The inspectors reviewed the following issues:
* Division 3 125VDC battery testing procedural adequacy;
* Unit 1 under vessel high temperature conditions;
* Generic Letter 08-01 emergency core cooling system gas entrainment assessment;
* 1C low pressure coolant injection (LPCI) suction valve thermal overload setpoint adjustment; and
* Core standby cooling system (CSCS) operability following hypothesized internal flooding with actual high cooling lake levels (greater than 701 elevation).
 
The inspectors selected these potential operability issues based on the risk-significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and Updated Safety Analysis Report (USAR) to the licensees evaluations, to determine whether the components or systems were operable.
 
Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.
 
Documents reviewed are listed in the Attachment to this report.
 
This operability inspection constituted five samples as defined in IP 71111.15-05
 
====b. Findings====
No findings of significance were identified. {{a|1R18}}
 
==1R18 Plant Modifications==
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18}}
{{IP sample|IP=IP 71111.18}}
...................................................................9
 
{{a|1R19}}
===.1 Temporary Plant Modifications===
====a. Inspection Scope====
The inspectors reviewed the containment ventilation (VP) chiller compressor trip bypass feature modification. They compared the temporary configuration changes and associated 10 CFR 50.59 screening and evaluation information against the design basis, the UFSAR, and the TS, as applicable, to verify that the modification did not affect the operability or availability of the affected system. The inspectors also compared the licensees information to operating experience information to ensure that lessons learned from other utilities had been incorporated into the licensees decision to implement the temporary modification. Lastly, the inspectors discussed the temporary modification with operations and engineering personnel to ensure that the individuals were aware of how extended operation with the temporary modification in place could impact overall plant performance. This temporary modification was approved for installation but had not yet been installed by the licensee by the close of this inspection period.
 
This inspection constituted one temporary modification sample as defined in IP 71111.18-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R19}}
 
==1R19 Post-Maintenance Testing (PMT)==
==1R19 Post-Maintenance Testing (PMT)==
{{IP sample|IP=IP 71111.19}}
{{IP sample|IP=IP 71111.19}}
............................................9
 
{{a|1R22}}
===.1 Post-Maintenance Testing===
====a. Inspection Scope====
The inspectors reviewed the following PMT activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:
* Drywell equipment drain sump outlet valve testing after emergent maintenance;
* 2B DG starting air compressor discharge check valve testing;
* 1C LPCI motor operated valve strokes following planned electrical breaker maintenance;
* 1B residual heat removal (RH) pump and valve run and strokes following planned electrical breaker maintenance; and
* 0 DG emergency fast start following a planned upkeep window.
 
These activities were selected based upon the structure, system, or components ability to impact risk. The inspectors evaluated these activities for the following (as applicable):
the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion), and test documentation was properly evaluated. The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with PMT to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted five PMT samples as defined in IP 71111.19-05.
 
====b. Findings====
No findings of significance were identified. {{a|1R22}}
 
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}
{{IP sample|IP=IP 71111.22}}
..............................................................10
 
{{a|1EP6}}
===.1 Surveillance Testing===
====a. Inspection Scope====
The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:
* LOS-R1-Q5; RCIC cold quick start (Routine);
* LOS-SQ-Q1 2B SLC pump and valve quarterly (Routine);
* LOS-VC-SR1 Control room and auxiliary electric equipment room ventilation pressurization surveillance (Routine);
* 2B RHR quarterly American Society of Mechanical Engineers surveillance (IST);and
* Unit 1 and Unit 2 drywell equipment drains (identified leakage) and drywell floor drains (unidentified leakage) surveillances (RCS).
 
The inspectors observed in plant activities and reviewed procedures and associated records to determine the following:
* did preconditioning occur;
* were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
* were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;
* plant equipment calibration was correct, accurate, and properly documented;
* as-left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the USAR, procedures, and applicable commitments;
* measuring and test equipment calibration was current;
* test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
* test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used;
* test data and results were accurate, complete, within limits, and valid;
* test equipment was removed after testing;
* where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers code, and reference values were consistent with the system design basis;
* where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;
* where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
* where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
* prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
* equipment was returned to a position or status required to support the performance of its safety functions; and
* all problems identified during the testing were appropriately documented and dispositioned in the CAP.
 
Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted three routine surveillance testing samples, one inservice testing sample, and one reactor coolant system leak detection inspection sample as defined in IP 71111.22, Sections -02 and -05.
 
====b. Findings====
No findings of significance were identified. {{a|1EP6}}
 
==1EP6 Drill Evaluation==
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06}}
{{IP sample|IP=IP 71114.06}}
.......................................................................11
 
===.1 Training Observation===
====a. Inspection Scope====
The inspector observed a simulator training evolution for licensed operators on September 16, 2008, which required emergency plan implementation by a licensee operations crew. This evolution was planned to be evaluated and included in performance indicator (PI) data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew.
 
The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that the licensee evaluators noted the same issues and entered them into the CAP. As part of the inspection, the inspectors reviewed the scenario package and other documents listed in the Attachment to this report.
 
This training inspection constituted one sample as defined in IP 71114.06-05.
 
====b. Findings====
No findings of significance were identified.


==RADIATION SAFETY==
==RADIATION SAFETY==
..............................................................................12 2OS1 Access Control to Radiologically Significant Areas (71121.01)................12 2OS2 As-Low-As-Is-Reasonably-Achievable (ALARA) Planning and Controls (71121.02)...............................................................................................13
===Cornerstone: Occupational Radiation Safety===
2OS1 Access Control to Radiologically Significant Areas (71121.01)
 
===.1 Plant Walkdowns and Radiation Work Permit (RWP) Reviews===
====a. Inspection Scope====
The inspectors assessed the adequacy of the licensees internal dose assessment process for internal exposures in excess of 50 millirem committed effective dose equivalent. The inspectors also reviewed the licensees physical and programmatic controls for highly activated and/or contaminated materials (non-fuel) stored within the spent fuel pool or other storage pools.
 
This occupational radiation safety plant walkdown and RWP review constituted two samples as defined in IP 71121.01-5.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Problem Identification and Resolution===
====a. Inspection Scope====
The inspectors reviewed licensee documentation packages for all PI events occurring since the last inspection to determine if any of these PI events involved dose rates greater than 25 R/hr at 30 centimeters or in excess of 500 R/hr at 1 meter. Barriers were evaluated for failure and to determine if there were any barriers left to prevent personnel access. Unintended exposures exceeding 100 millirem total effective dose equivalent (or 5 Rem shallow dose equivalent or 1.5 Rem lens dose equivalent) were evaluated to determine if there were any regulatory overexposures or if there was a substantial potential for an overexposure.
 
This radiation safety licensee documentation inspection constituted one sample as defined in IP 71121.01-5.
 
====b. Findings====
No findings of significance were identified.
2OS2 As-Low-As-Is-Reasonably-Achievable (ALARA) Planning and Controls (71121.02)
 
===.1 Declared Pregnant Workers===
====a. Inspection Scope====
The inspectors reviewed dose records of declared pregnant workers for the current assessment period to verify that the exposure results and monitoring controls employed by the licensee complied with the requirements of 10 CFR Part 20. The inspectors reviewed the licensees program for declared pregnant workers. The inspectors evaluated if that program complied with the requirements of 10 CFR Part 20.
 
This ALARA declared pregnant workers inspection constituted one required sample as defined in IP 71121.02-5.
 
====b. Findings====
No findings of significance were identified.


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
................................................................................13
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
{{IP sample|IP=IP 71151}}
..............................................13
 
{{a|4OA2}}
===.1 Unplanned Scrams per 7000 Critical Hours===
====a. Inspection Scope====
The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical Hours PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5 were used. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports and NRC Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.
 
Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted two unplanned scrams per 7000 critical hours samples as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Unplanned Scrams with Complications===
====a. Inspection Scope====
The inspectors sampled licensee submittals for the Unplanned Scrams with Complications PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports and NRC Integrated Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted two unplanned scrams with complications samples as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified.
 
===.3 Unplanned Transients per 7000 Critical Hours===
====a. Inspection Scope====
The inspectors sampled licensee submittals for the Unplanned Transients per 7000 Critical Hours PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, maintenance rule records, event reports and NRC Integrated Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted two unplanned transients per 7000 critical hours samples as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified.
 
===.4 Reactor Coolant System (RCS) Specific Activity===
====a. Inspection Scope====
The inspectors sampled licensee submittals for the RCS Specific Activity PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees RCS chemistry samples, TS requirements, issue reports, and event reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals.
 
The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator, and none were identified. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted two RCS specific activity samples as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified.
 
===.5 Reactor Coolant System Leakage===
====a. Inspection Scope====
The inspectors sampled licensee submittals for the RCS Leakage PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator logs, RCS leakage tracking data, issue reports, event reports and NRC Integrated Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted two RCS leakage samples as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified.
 
===.6 Occupational Exposure Control Effectiveness===
====a. Inspection Scope====
The inspectors sampled licensee submittals for the Occupational Radiological Occurrences PI for the period from the 3rd quarter 2007 through the 2nd quarter 2008.
 
To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees assessment of the PI for occupational radiation safety to determine if indicator related data was adequately assessed and reported. To assess the adequacy of the licensees PI data collection and analyses, the inspectors discussed with radiation protection staff, the scope and breadth of its data review, and the results of those reviews. The inspectors independently reviewed electronic dosimetry dose rate and accumulated dose alarm and dose reports and the dose assignments for any intakes that occurred during the time period reviewed to determine if there were potentially unrecognized occurrences. The inspectors also conducted walkdowns of numerous locked high and very high radiation area entrances to determine the adequacy of the controls in place for these areas. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one occupational radiological occurrences sample as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified.
 
===.7 Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent===
Occurrences
 
====a. Inspection Scope====
The inspectors sampled licensee submittals for the Radiological Effluent TS (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent Occurrences PI for the period from the 3rd quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees issue report database and selected individual reports generated since this indicator was last reviewed to identify any potential occurrences such as unmonitored, uncontrolled, or improperly calculated effluent releases that may have impacted offsite dose. The inspectors reviewed gaseous effluent summary data and the results of associated offsite dose calculations for selected dates between from the third quarter 2007 through the second quarter 2008, to determine if indicator results were accurately reported. The inspectors also reviewed the licensees methods for quantifying gaseous and liquid effluents and determining effluent dose. Additionally, the inspectors reviewed the licensees historical 10 CFR 50.75(g) file and selectively reviewed the licensees analysis for discharge pathways resulting from a spill, leak, or unexpected liquid discharge focusing on those incidents which occurred over the last few years. Documents reviewed are listed in the Attachment to this report.
 
This inspection constituted one RETS/ODCM radiological effluent occurrences sample as defined in IP 71151-05.
 
====b. Findings====
No findings of significance were identified. {{a|4OA2}}
 
==4OA2 Identification and Resolution of Problems==
==4OA2 Identification and Resolution of Problems==
{{IP sample|IP=IP 71152}}
{{IP sample|IP=IP 71152}}
...................................17
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection
{{a|4OA3}}
 
===.1 Routine Review of items Entered Into the CAP===
====a. Scope====
As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Attributes reviewed included: the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and that previous occurrences reviews were proper and adequate. Also, the classification, prioritization, focus, and timeliness of corrective actions were reviewed to ensure they were commensurate with safety and sufficient to prevent recurrence of the issue. Minor issues entered into the licensees CAP as a result of the inspectors observations are included in the attached list of documents reviewed.
 
These routine reviews from IP 71152 for the identification and resolution of problems did not constitute any additional inspection samples. Instead, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.
 
====b. Findings====
No findings of significance were identified.
 
===.2 Daily CAP Reviews===
====a. Scope====
In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished through inspection of the stations daily condition report packages.
 
These daily reviews were performed as defined in IP 71152 as part of the inspectors daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.
 
====b. Findings====
No findings of significance were identified.
 
===.3 Annual Review: Operator Workarounds (OWA)===
====a. Scope====
The inspectors evaluated the licensees implementation of their process used to identify, document, track, and resolve operational challenges. Inspection activities included, but were not limited to, a review of the cumulative effects of the OWAs on system availability and the potential for improper operation of the system, for potential impacts on multiple systems, and on the ability of operators to respond to plant transients or accidents.
 
The inspectors performed a review of the cumulative effects of OWAs. The documents listed in the Attachment were reviewed to accomplish the objectives of the inspection procedure. The inspectors also reviewed operator challenges, which create an obstacle to normal plant operation, rather than the more severe obstacle to safe plant operation created by an OWA. The inspectors reviewed both current and historical operational challenge records to determine whether the licensee was identifying operator challenges at an appropriate threshold, had entered them into their CAP and proposed or implemented appropriate and timely corrective actions which addressed each issue.
 
Reviews were conducted to determine if any operator challenge could increase the possibility of an Initiating Event, if the challenge was contrary to training, required a change from long-standing operational practices, or created the potential for inappropriate compensatory actions. Additionally, all temporary modifications were reviewed to identify any potential effect on the functionality of Mitigating Systems, impaired access to equipment, or required equipment uses for which the equipment was not designed. Daily plant and equipment status logs, degraded instrument logs, and operator aids or tools being used to compensate for material deficiencies were also assessed to identify any potential sources of unidentified operator workarounds. In addition, interviews were conducted with equipment operators and licensed control room operators to determine if longstanding workarounds existed and had in turn been proceduralized into a part of accepted practice.
 
This operator workarounds annual inspection review constituted one sample as defined in IP 71152.
 
====b. Findings====
No findings of significance were identified.
 
===.4 Annual Review: Safety-Related Procedure Changes===
====a. Scope====
The inspectors reviewed a sample of approximately 100 issue reports associated with revisions to plant procedures that were associated with safety-related components or emergency operations to evaluate whether the licensees process to identify, prioritize and resolve changes needed for those procedures was adequate. Specifically, the inspectors selected procedural changes for which the due dates were moved by more than six months and revisions that would directly impact Emergency Operating Procedures. The inspectors evaluated the validity of extending the due date on a needed revision of a safety-related procedure and ensured the revisions were timely and commensurate with the safety significance of the issue. Additionally, the inspectors verified that established corrective actions by the licensee for the safety-related procedures were appropriately focused to correct the problem.
 
b.
 
Observations The inspectors noted that the licensee properly identified deficiencies in their procedures; however, the process for prioritizing and resolving the changes lacked some organization. Specifically, it was the responsibility of a few individuals from the Operations and Training departments to ensure that these procedure revisions were performed in a timely manner. The inspectors noticed that there was not a formal threshold or process to establish priorities for procedures needing modification other than personal discretion and foreseen or unforeseen events. Some examples of events that influenced the establishment of due dates were refueling outages, major equipment malfunctions and other NRC inspections.
 
The inspectors observed that the events that influenced the priority category and original due dates for the issue reports were also used as basis for adjusting the due dates when the actions required could not be completed in time. Additionally, the inspectors noted that in most of the issue reports with postponements, no written justification was provided for deferring the completion date. The inspectors interviewed the personnel in charge of these procedure changes to gather the information on each issue and assess whether the delays were handled in accordance with safety significance. From the sample selected, approximately 20 percent of the procedure changes required were deferred from the original due dates several times and in some cases they were pushed back by more than 6 months up to a year.
 
The inspectors concluded that the licensee identified necessary procedural changes commensurate with safety. However, due to the workload of personnel tasked with these changes, the prioritization and execution of these procedural revisions could improve by performing a more structured significance determination and by justifying due date rescheduling to better track the program. The inspectors did not identify any issues where the resolution timeliness of the issue report compromised the safety of plant operation.
 
This safety related procedural changes review constituted one inspection sample as defined in IP 71152.
 
====c. Findings====
No findings of significance were identified. {{a|4OA3}}
 
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
==4OA3 Follow-Up of Events and Notices of Enforcement Discretion==
{{IP sample|IP=IP 71153}}
{{IP sample|IP=IP 71153}}
......19
 
{{a|4OA5}}
===.1 (Closed) LER 05000374/2008001-00, High Pressure Core Spray System Declared===
==4OA5 Other.......................................................................................................20 4OA6==
Inoperable Due to Failed Room Ventilation Supply Fan
Management Meetings............................................................................21 4OA7 Licensee-Identified Violations..................................................................21
 
====a. Inspection Scope====
On June 11, 2008, the supply fan for the Division 3 switchgear room ventilation system (VD) tripped unexpectedly. Division 3 switchgear supports the high pressure core spray (HPCS) system. High pressure core spray remained available to inject into the reactor vessel if needed, but was declared inoperable due to potential room heat-up with the rooms ventilation failed. As HPCS is a single train system, this failure resulted in a complete loss of system function, requiring the licensee to make an eight hour notification to the NRC under 10 CFR 50.72(b)(3)(v)(D). This event was also classified as a Safety System Functional Failure. The failure mechanism was identified by the licensee as a phase to ground short on the fans motor winding. The licensee determined the apparent cause of the motor winding failure to be a lack of a time-based refurbishment/replacement program for high duty cycle (continuously run) motors. The motor in question received periodic greasing of its bearings and quarterly vibration analysis, but no refurbishment/ replacement schedule had been established. This component was from original construction (approximately 25 years old) and vendor environmental qualification records analyzed that this component was expected to last for the licensed lifetime of the plant (40 years).
 
During the apparent cause investigation, the licensee identified Electric Power Research Institute (EPRI) guidance that revealed that high duty cycle motors in low power applications, such as ventilation fans, have been known to show signs of electrical degradation beginning at approximately 20 years of service. As a corrective action, the licensee established a 20 year refurbishment/replacement criteria for the supply fan in question. The licensee performed an extent of condition review of all 480 volt motors site wide extending the 20 year criterion to all critical (safety/risk significant), high duty cycle, single train, and short duration TS shutdown time clock (less than or equal to seven days) motor driven components. This expanded the motor population to four total components (the supply and return fans associated with each units Division 3 VD system). The inspectors review of the EPRI operating experience showed it to be general in nature, lacking the specificity that would reasonably cause the licensee to reevaluate previous vendor lifetime qualification data and as such the failure to establish a refurbishment/replacement criteria based on industry experience was not considered a performance deficiency. Documents reviewed in this inspection are listed in the
. This LER is closed.
 
This event follow-up review constituted one sample as defined in Inspection Procedure 71153-05.
 
====b. Findings====
No findings of significance were identified.
{{a|4OA5}}
 
==4OA5 Other==
===Cornerstone: Physical Protection===
===.1 Quarterly Resident Inspector Observations of Security Personnel and Activities===
====a. Inspection Scope====
During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.
 
These observations took place during both normal and off-normal plant working hours.
 
The inspectors also reviewed a report of the results of a survey of the site security organization relative to its safety conscious work environment. The inspectors considered whether the surveys were conducted in a manner that encouraged candid and honest feedback. The results were reviewed to determine whether adequate number of staff responded to the survey. The inspectors also reviewed Exelons self-assessment of the survey results and verified that any issues or areas for improvement were entered into the CAP for resolution.
 
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors normal plant status review and inspection activities.
 
====b. Findings====
No findings of significance were identified.
{{a|4OA6}}
 
==4OA6 Management Meetings==
===.1===
===Exit Meeting Summary===
On October 2, 2008, the inspectors presented the inspection results to Site Vice President, Mr. Daniel Enright, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.
 
===.2 Interim Exit Meetings===
Interim exits were conducted for:
* The results of the heat sink performance inspection with the Plant Manager, Mr. D. Rhoades, on July 25, 2008; and
* The results of the radiation protection inspection with the Plant Manager, Mr. D. Rhodes, on August 29, 2008.
 
The inspectors confirmed that none of the potential report input discussed was considered proprietary.
 
{{a|4OA7}}
 
==4OA7 Licensee-Identified Violations==
None.
 
ATTACHMENT:


=SUPPLEMENTAL INFORMATION=
=SUPPLEMENTAL INFORMATION=


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
..................................................................................................1
Licensee
: [[contact::D. Enright]], Site Vice President
: [[contact::D. Rhoades]], Plant Manager
: [[contact::J. Bashor]], Site Engineering Director
: [[contact::L. Blunk]], Operations Training Manager
: [[contact::S. Wilkinson]], Chemistry Manager
: [[contact::H. Do]], Corporate Inservice Inspection Manager
: [[contact::B. Ginter]], Engineering Programs Manager
: [[contact::F. Gogliotti]], System Engineering Senior Manager
: [[contact::W. Hilton]], Engineering Supervisor - Mechanical/Structural
: [[contact::K. Ihnen]], Nuclear Oversight Manager
: [[contact::A. Kochis]], Inservice Inspection Engineer
: [[contact::R. Leasure]], Radiation Protection Manager
: [[contact::S. Marik]], Operations Director
: [[contact::J. Miller]], NDE Level III
: [[contact::B. Rash]], Maintenance Director
: [[contact::J. Rommel]], Design Engineering Senior Manager
: [[contact::K. Rusley]], Emergency Preparedness Manager
: [[contact::J. Shields]], Inservice Inspection Program Supervisor
: [[contact::T. Simpkin]], Regulatory Assurance Manager
: [[contact::H. Vinyard]], Shift Operations Superintendent
: [[contact::G. Wilhelmsen]], Design Manager
: [[contact::J. White]], Site Training Director
: [[contact::C. Wilson]], Station Security Manager
: [[contact::D. Amezaga]], GL 89-13 Program Owner
: [[contact::J.C. Feeney]], NOS Lead Assessor
: [[contact::D. Henly]], Design Engineer
Nuclear Regulatory Commission
: [[contact::K. Riemer]], Chief, Reactor Projects Branch 2
 
==LIST OF ITEMS==
==LIST OF ITEMS==
OPENED, CLOSED AND DISCUSSED........................................................1
===OPENED, CLOSED AND DISCUSSED===
===Opened===
None.  
 
===Closed===
: 05000374/2008001-00 LER High Pressure Core Spray System Declared Inoperable Due to Failed Room Ventilation Supply Fan (4OA3)
 
===Discussed===
None.  
 
==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
.......................................................................................2
 
==LIST OF ACRONYMS==
: [[US]] [[]]
ED ...............................................................................................19
Enclosure
: [[SUMMAR]] [[Y]]
: [[OF]] [[]]
: [[FINDIN]] [[]]
: [[GS]] [[]]
: [[IR]] [[05000373/2008004, 05000374/2008004; 7/01/2008 - 9/30/2008; LaSalle County Station, Units 1 & 2; routine integrated report. The inspection was conducted by U.S. Nuclear Regulatory Commission (]]
NRC) resident inspectors and regional inspectors. The report covers a three-month period of resident inspection, and announced inspection in the areas of health physics, heat sink performance,
and diesel generator performance testing. No findings of significance were identified. The
: [[NRC]] [['s program for overseeing the safe operation of commercial nuclear power reactors is described in]]
NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000. Inspector-Identified and Self-Revealed Findings No findings of significance were identified. Licensee-Identified Violations No violations of significance were identified.
Enclosure
: [[REPORT]] [[]]
DETAILS Summary of Plant Status Unit 1
The unit began the inspection period operating at full power. On July 20, 2008, the unit was reduced to 82 percent for motor driven reactor feed pump and main turbine valve surveillance testing. The unit returned to full power that same day. On September 6, 2008, power was
reduced to approximately 66 percent to perform control rod sequence exchange and scram time testing. Operation at full power resumed on September 7, 2008. On September 28, 2008, the unit was shutdown to perform repairs of a hydrogen leak on the main generator housing. The unit remained in mode 3 (hot shutdown) for the rest of the inspection period. Unit 2 The unit began the inspection period operating at full power. On July 27, 2008, power was reduced to approximately 62 percent for channel distortion testing of all the interior rods. The unit was returned to full power that same day. On August 30, 2008, the unit commenced a reduction in power to 53 percent for control rod sequence exchange and feedwater pump turbine surveillances. The unit was returned to full power on August 31, 2008, where it remained until September 26, 2008. At this time, power was reduced to 55 percent for power suppression testing, control rod
: [[SCR]] [[]]
AM time testing and channel distortion testing. Full power
was restored on September 29, 2008, and the unit remained operating at or near full power for the rest of the inspection period. 1.
: [[REACTO]] [[R]]
SAFETY Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness 1R04 Equipment Alignment (71111.04) .1 Quarterly Partial System Walkdowns a. Inspection Scope The inspectors performed partial system walkdowns of the following risk-significant systems: * Unit 2 low pressure core spray (LPCS); * 2A standby liquid control (SLC) with 2B out-of-service; and * 1A and 2A diesel generators (DG) and support systems with the 0 DG out of service. The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted
to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, outstanding work orders, condition reports, and the
Enclosure impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The
inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program (CAP) with the appropriate significance characterization. Documents reviewed are listed in the Attachment. These activities constituted three partial system walkdown samples as defined in Inspection Procedure (IP) 71111.04-05. b. Findings No findings of significance were identified. .2 Semi-Annual Complete System Walkdown a. Inspection Scope On August 27 through August 29, 2008, the inspectors performed a complete system alignment inspection of the fire protection system to verify the functional capability of the system. This system was selected because it was considered risk-significant in the licensee's probabilistic risk assessment. The inspectors walked down the system to review mechanical and electrical equipment line ups, electrical power availability, system pressure and temperature indications, as appropriate, component labeling, component
lubrication, component and equipment cooling, hangers and supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation. A review of a sample of past and outstanding work orders (WOs) was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the CAP database to ensure that system
equipment alignment problems were being identified and appropriately resolved. Documents reviewed are listed in the Attachment to this report. These activities constituted one complete system walkdown sample as defined in IP 71111.04-05. b. Findings No findings of significance were identified.
Enclosure 1R05 Fire Protection (71111.05) .1 Routine Resident Inspector Tours (71111.05Q) a. Inspection Scope The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas: * Fire Zone 7B3
: [[0 DG]] [[Room; * Fire Zone 4F2 Unit 2 Division 1 switchgear; * Fire Zone 2G Unit 1 reactor building 710'; * Fire Zone 214 Unit 1 reactor core isolation cooling (]]
RCIC)/LPCS; and * Fire Zone 2B1 Unit 1 reactor building 820'. The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for out-of-service, degraded or inoperable fire
protection equipment, systems, or features in accordance with the licensee's fire plan. The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plant's Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plant's ability to respond to a security event. Using
the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified
during the inspection were entered into the licensee's
: [[CAP.]] [[Documents reviewed are listed in the Attachment to this report. These activities constituted five quarterly fire protection inspection samples as defined in]]
IP 71111.05-05. b. Findings No findings of significance were identified. 1R07 Heat Sink Performance (71111.07T) .1 Triennial Review of Heat Sink Performance a. Inspection Scope The inspectors reviewed operability determinations, completed surveillances, vendor manual information, associated calculations, performance test results and cooler inspection results associated with the 2B Residual Heat Removal (RHR) heat exchanger
and the
: [[DG]] [[common to both units (0]]
DG) heat exchanger. These heat exchangers were
Enclosure chosen based on their risk significance in the licensee's probabilistic safety analysis, their important safety-related mitigating system support functions and their relatively low margin. For the 2B
: [[RHR]] [[and the 0]]
DG heat exchangers, the inspectors verified that testing, inspection, maintenance, and monitoring of biotic fouling and macrofouling programs were adequate to ensure proper heat transfer. This was accomplished by verifying the
test method used was consistent with accepted industry practices, or equivalent, the test conditions were consistent with the selected methodology, the test acceptance criteria were consistent with the design basis values, and results of heat exchanger performance testing. The inspectors also verified that the test results appropriately considered differences between testing conditions and design conditions, the frequency
of testing based on trending of test results was sufficient to detect degradation prior to loss of heat removal capabilities below design basis values and test results considered test instrument inaccuracies and differences. For the 2B
: [[RHR]] [[and the 0]]
DG heat exchanger, the inspectors reviewed the methods and results of heat exchanger performance inspections. The inspectors verified the methods used to inspect and clean heat exchangers were consistent with as-found conditions identified and expected degradation trends and industry standards, the
licensee's inspection and cleaning activities had established acceptance criteria consistent with industry standards, and the as-found results were recorded, evaluated, and appropriately dispositioned such that the as-left condition was acceptable. The inspectors verified the performance of the ultimate heat sink (UHS) and their subcomponents, including piping, intake screens, pumps, and valves, by tests or visual
inspection to ensure availability and accessibility to the in-plant cooling water systems. The inspectors reviewed the results of the licensee's inspection of the UHS weirs or excavations. The inspectors verified that identified settlement or movement indicating loss of structural integrity and/or capacity was appropriately evaluated and dispositioned by the licensee. In addition, the inspectors verified the licensee ensured sufficient
reservoir capacity by trending and removing debris or sediment buildup in the UHS. The inspectors performed a system walkdown of the service water intake structure to verify the licensee's assessment on structural integrity and component functionality. This included the verification that licensee ensured proper functioning of traveling screens and strainers, and structural integrity of component mounts. In addition, the
inspectors verified that service water pump bay silt accumulation is monitored, trended, and maintained at an acceptable level by the licensee, and that water level instruments are functional and routinely monitored. The inspectors also verified the licensee's ability to ensure functionality during adverse weather conditions. In addition, the inspectors reviewed condition reports related to the heat exchangers/coolers and heat sink performance issues to verify that the licensee had an appropriate threshold for identifying issues and to evaluate the effectiveness of the corrective actions. The documents reviewed are included in the Attachment to this report. These inspection activities constituted two heat sink inspection samples as defined in IP 71111.07-05.
Enclosure b. Findings No findings of significance were identified 1R11 Licensed Operator Requalification Program (71111.11) .1 Resident Inspector Quarterly Review (71111.11Q) a. Inspection Scope On September 16, 2008, the inspectors observed a crew of licensed operators in the plant's simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas: * licensed operator performance; * crew's clarity and formality of communications; * ability to take timely actions in the conservative direction; * prioritization, interpretation, and verification of annunciator alarms; * correct use and implementation of abnormal and emergency procedures; * control board manipulations; * oversight and direction from supervisors; and * ability to identify and implement appropriate
: [[TS]] [[actions and Emergency Plan actions and notifications. The crew's performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report. This inspection constituted one quarterly licensed operator requalification program sample as defined in]]
IP 71111.11. b. Findings No findings of significance were identified. 1R12 Maintenance Effectiveness (71111.12) .1 Routine Quarterly Evaluations (71111.12Q) a. Inspection Scope The inspectors evaluated degraded performance issues involving the following risk significant systems/components: * Circulating water system; and * Maintenance rule functional failure assessment for control rod drive (CRD) pressure control bypass valve 1C11-F004.
Enclosure The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensee's actions to address system performance or condition problems in terms of the following: * implementing appropriate work practices; * identifying and addressing common cause failures; * scoping of systems in accordance with the Code of Federal Regulations (CFR)
: [[10 CFR]] [[50.65(b) of the maintenance rule; * characterizing system reliability issues for performance; * charging unavailability for performance; * trending key parameters for condition monitoring; * ensuring 10]]
CFR 50.65(a)(1) or (a)(2) classification or re-classification; and * verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1). The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance
effectiveness issues were entered into the
: [[CAP]] [[with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report. This inspection constituted two quarterly maintenance effectiveness samples as defined in]]
: [[IP]] [[71111.12-05. b. Findings No findings of significance were identified. 1R13  Maintenance Risk Assessments and Emergent Work Control (71111.13) .1 Maintenance Risk Assessments and Emergent Work Control a. Inspection Scope The inspectors reviewed the licensee's evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work: * Unit 1 motor-driven reactor feed pump protected pathway; * Unit 2 electro-hydraulic control (EHC) filter emergent replacement; * 2B non-essential service water jockey pump suction pipe thru-wall flaw; and * 1B]]
: [[DG]] [[protected pathway. These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10]]
CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensee's
Enclosure probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed
: [[TS]] [[requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met. These maintenance risk assessments and emergent work control activities constituted four samples as defined in]]
: [[IP]] [[71111.13-05. b. Findings No findings of significance were identified. 1R15 Operability Evaluations (71111.15) .1 Operability Evaluations a. Inspection Scope The inspectors reviewed the following issues: * Division 3]]
: [[125VDC]] [[battery testing procedural adequacy; * Unit 1 under vessel high temperature conditions; * Generic Letter 08-01 emergency core cooling system gas entrainment assessment; * 1C low pressure coolant injection (]]
: [[LPCI]] [[) suction valve thermal overload setpoint adjustment; and  * Core standby cooling system (CSCS) operability following hypothesized internal flooding with actual high cooling lake levels (greater than 701' elevation). The inspectors selected these potential operability issues based on the risk-significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that]]
: [[TS]] [[operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the]]
TS and Updated Safety Analysis Report (USAR) to the
licensee's evaluations, to determine whether the components or systems were operable. Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.
Documents reviewed are listed in the Attachment to this report. This operability inspection constituted five samples as defined in IP 71111.15-05 b. Findings No findings of significance were identified.
Enclosure 1R18 Plant Modifications (71111.18) .1 Temporary Plant Modifications a. Inspection Scope The inspectors reviewed the containment ventilation (VP) chiller compressor trip bypass feature modification. They compared the temporary configuration changes and associated 10 CFR 50.59 screening and evaluation information against the design basis,
the
: [[UFSAR]] [[, and the]]
TS, as applicable, to verify that the modification did not affect the operability or availability of the affected system. The inspectors also compared the licensee's information to operating experience information to ensure that lessons learned from other utilities had been incorporated into the licensee's decision to implement the temporary modification. Lastly, the inspectors discussed the temporary modification with
operations and engineering personnel to ensure that the individuals were aware of how extended operation with the temporary modification in place could impact overall plant performance. This temporary modification was approved for installation but had not yet been installed by the licensee by the close of this inspection period. This inspection constituted one temporary modification sample as defined in
: [[IP]] [[71111.18-05. b. Findings No findings of significance were identified. 1R19 Post-Maintenance Testing (]]
: [[PMT]] [[) (71111.19) .1 Post-Maintenance Testing a. Inspection Scope The inspectors reviewed the following]]
: [[PMT]] [[activities to verify that procedures and test activities were adequate to ensure system operability and functional capability: * Drywell equipment drain sump outlet valve testing after emergent maintenance; * 2B]]
: [[DG]] [[starting air compressor discharge check valve testing; * 1C]]
: [[LPCI]] [[motor operated valve strokes following planned electrical breaker maintenance; * 1B residual heat removal (]]
RH) pump and valve run and strokes following planned electrical breaker maintenance; and * 0 DG emergency fast start following a planned upkeep window. These activities were selected based upon the structure, system, or component's ability to impact risk. The inspectors evaluated these activities for the following (as applicable):
the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers
required for test performance were properly removed after test completion), and test
Enclosure documentation was properly evaluated. The inspectors evaluated the activities against
: [[TS]] [[, the]]
: [[UFSAR]] [[,]]
: [[10 CFR]] [[Part 50 requirements, licensee procedures, and various]]
: [[NRC]] [[generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with]]
: [[PMT]] [[to determine whether the licensee was identifying problems and entering them in the]]
CAP and that the problems
were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report. This inspection constituted five
: [[PMT]] [[samples as defined in]]
: [[IP]] [[71111.19-05. b. Findings No findings of significance were identified. 1R22 Surveillance Testing (71111.22) .1 Surveillance Testing a. Inspection Scope The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and]]
: [[TS]] [[requirements: *]]
: [[LOS]] [[-R1-Q5;]]
: [[RCIC]] [[cold quick start (Routine); *]]
: [[LOS]] [[-SQ-Q1 2B]]
: [[SLC]] [[pump and valve quarterly (Routine); *]]
: [[LOS]] [[-VC-SR1 Control room and auxiliary electric equipment room ventilation pressurization surveillance (Routine); * 2B]]
: [[RHR]] [[quarterly American Society of Mechanical Engineers surveillance (]]
: [[IST]] [[); and * Unit 1 and Unit 2 drywell equipment drains (identified leakage) and drywell floor drains (unidentified leakage) surveillances (RCS). The inspectors observed in plant activities and reviewed procedures and associated records to determine the following:  * did preconditioning occur;  * were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing; * were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis; * plant equipment calibration was correct, accurate, and properly documented; * as-left setpoints were within required ranges; and the calibration frequency were in accordance with]]
: [[TS]] [[s, the]]
USAR, procedures, and applicable commitments; * measuring and test equipment calibration was current; * test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
Enclosure * test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored
where used; * test data and results were accurate, complete, within limits, and valid; * test equipment was removed after testing; * where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers code, and reference values were consistent with the
system design basis; * where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable; * where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure; * where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished; * prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test; * equipment was returned to a position or status required to support the performance of its safety functions; and * all problems identified during the testing were appropriately documented and dispositioned in the CAP. Documents reviewed are listed in the Attachment to this report. This inspection constituted three routine surveillance testing samples, one inservice testing sample, and one reactor coolant system leak detection inspection sample as
defined in
: [[IP]] [[71111.22, Sections -02 and -05. b. Findings No findings of significance were identified. 1]]
EP6 Drill Evaluation (71114.06) .1 Training Observation a. Inspection Scope  The inspector observed a simulator training evolution for licensed operators on September 16, 2008, which required emergency plan implementation by a licensee operations crew. This evolution was planned to be evaluated and included in performance indicator (PI) data regarding drill and exercise performance. The
inspectors observed event classification and notification activities performed by the crew. The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors' activities was to note any weaknesses and deficiencies in the crew's performance and ensure that the licensee evaluators noted the same issues and entered them into the CAP. As part of the inspection, the inspectors reviewed the scenario
package and other documents listed in the Attachment to this report.
Enclosure This training inspection constituted one sample as defined in
: [[IP]] [[71114.06-05. b. Findings No findings of significance were identified. 2.]]
: [[RADIAT]] [[ION]]
: [[SAFETY]] [[Cornerstone:  Occupational Radiation Safety 2]]
OS1 Access Control to Radiologically Significant Areas (71121.01) .1 Plant Walkdowns and Radiation Work Permit (RWP) Reviews a. Inspection Scope The inspectors assessed the adequacy of the licensee's internal dose assessment process for internal exposures in excess of 50 millirem committed effective dose equivalent. The inspectors also reviewed the licensee's physical and programmatic
controls for highly activated and/or contaminated materials (non-fuel) stored within the spent fuel pool or other storage pools. This occupational radiation safety plant walkdown and
: [[RWP]] [[review constituted two samples as defined in]]
: [[IP]] [[71121.01-5. b. Findings No findings of significance were identified.  .2 Problem Identification and Resolution a. Inspection Scope The inspectors reviewed licensee documentation packages for all]]
: [[PI]] [[events occurring since the last inspection to determine if any of these]]
PI events involved dose rates greater than 25 R/hr at 30 centimeters or in excess of 500 R/hr at 1 meter. Barriers were evaluated for failure and to determine if there were any barriers left to prevent
personnel access. Unintended exposures exceeding 100 millirem total effective dose equivalent (or 5 Rem shallow dose equivalent or 1.5 Rem lens dose equivalent) were evaluated to determine if there were any regulatory overexposures or if there was a substantial potential for an overexposure. This radiation safety licensee documentation inspection constituted one sample as defined in IP 71121.01-5. b. Findings No findings of significance were identified.
Enclosure
: [[2OS]] [[2 As-Low-As-Is-Reasonably-Achievable (]]
ALARA) Planning and Controls (71121.02) .1 Declared Pregnant Workers a. Inspection Scope The inspectors reviewed dose records of declared pregnant workers for the current assessment period to verify that the exposure results and monitoring controls employed by the licensee complied with the requirements of 10 CFR Part 20. The inspectors
reviewed the licensee's program for declared pregnant workers. The inspectors evaluated if that program complied with the requirements of
: [[10 CFR]] [[Part 20. This]]
: [[ALARA]] [[declared pregnant workers inspection constituted one required sample as defined in]]
: [[IP]] [[71121.02-5. b. Findings No findings of significance were identified. 4.]]
: [[OTHER]] [[]]
: [[ACTIVI]] [[]]
: [[TIES]] [[]]
: [[4OA]] [[1 Performance Indicator Verification (71151) .1 Unplanned Scrams per 7000 Critical Hours a. Inspection Scope The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical Hours]]
: [[PI]] [[for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the]]
: [[PI]] [[data reported during those periods,]]
PI definitions and guidance contained in the Nuclear Energy Institute (NEI) Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5 were used. The inspectors reviewed the licensee's operator narrative logs, issue reports, event reports and NRC Inspection Reports for the period of October 2007 through
June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the
: [[PI]] [[data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report. This inspection constituted two unplanned scrams per 7000 critical hours samples as defined in]]
IP 71151-05. b. Findings No findings of significance were identified. .2 Unplanned Scrams with Complications a. Inspection Scope The inspectors sampled licensee submittals for the Unplanned Scrams with Complications PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through
Enclosure the 2nd quarter 2008. To determine the accuracy of the
: [[PI]] [[data reported during those periods,]]
: [[PI]] [[definitions and guidance contained in the]]
: [[NEI]] [[Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, were used. The inspectors reviewed the licensee's operator narrative logs, issue reports, event reports and]]
NRC Integrated Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensee's
issue report database to determine if any problems had been identified with the
: [[PI]] [[data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report. This inspection constituted two unplanned scrams with complications samples as defined in]]
: [[IP]] [[71151-05. b. Findings No findings of significance were identified. .3 Unplanned Transients per 7000 Critical Hours a. Inspection Scope The inspectors sampled licensee submittals for the Unplanned Transients per 7000 Critical Hours]]
: [[PI]] [[for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the]]
: [[PI]] [[data reported during those periods,]]
: [[PI]] [[definitions and guidance contained in the]]
NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, were used. The inspectors reviewed the licensee's operator narrative logs, issue reports, maintenance rule records, event reports and NRC Integrated Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also
reviewed the licensee's issue report database to determine if any problems had been identified with the
: [[PI]] [[data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report. This inspection constituted two unplanned transients per 7000 critical hours samples as defined in]]
: [[IP]] [[71151-05. b. Findings No findings of significance were identified. .4 Reactor Coolant System (RCS) Specific Activity a. Inspection Scope The inspectors sampled licensee submittals for the]]
: [[RCS]] [[Specific Activity]]
: [[PI]] [[for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the]]
: [[PI]] [[data reported during those periods,]]
: [[PI]] [[definitions and guidance contained in the]]
: [[NEI]] [[Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, were used. The inspectors reviewed the licensee's]]
RCS chemistry samples, TS requirements, issue reports, and event reports for the
period of October 2007 through June 2008 to validate the accuracy of the submittals.
Enclosure The inspectors also reviewed the licensee's issue report database to determine if any problems had been identified with the
: [[PI]] [[data collected or transmitted for this indicator, and none were identified. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Documents reviewed are listed in the Attachment to this report. This inspection constituted two]]
: [[RCS]] [[specific activity samples as defined in]]
: [[IP]] [[71151-05. b. Findings No findings of significance were identified. .5 Reactor Coolant System Leakage a. Inspection Scope The inspectors sampled licensee submittals for the]]
: [[RCS]] [[Leakage]]
: [[PI]] [[for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the]]
: [[PI]] [[data reported during those periods,]]
: [[PI]] [[definitions and guidance contained in the]]
: [[NEI]] [[Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, were used. The inspectors reviewed the licensee's operator logs,]]
: [[RCS]] [[leakage tracking data, issue reports, event reports and]]
NRC Integrated Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensee's
issue report database to determine if any problems had been identified with the
: [[PI]] [[data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report. This inspection constituted two]]
: [[RCS]] [[leakage samples as defined in]]
: [[IP]] [[71151-05. b. Findings No findings of significance were identified.  .6 Occupational Exposure Control Effectiveness a. Inspection Scope The inspectors sampled licensee submittals for the Occupational Radiological Occurrences]]
PI for the period from the 3rd quarter 2007 through the 2nd quarter 2008.
To determine the accuracy of the
: [[PI]] [[data reported during those periods,]]
: [[PI]] [[definitions and guidance contained in the]]
: [[NEI]] [[Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, were used. The inspectors reviewed the licensee's assessment of the]]
PI for occupational radiation safety to determine if indicator related data was adequately assessed and reported. To assess the adequacy of the
licensee's PI data collection and analyses, the inspectors discussed with radiation protection staff, the scope and breadth of its data review, and the results of those reviews. The inspectors independently reviewed electronic dosimetry dose rate and accumulated dose alarm and dose reports and the dose assignments for any intakes that occurred during the time period reviewed to determine if there were potentially
unrecognized occurrences. The inspectors also conducted walkdowns of numerous
Enclosure locked high and very high radiation area entrances to determine the adequacy of the controls in place for these areas. Documents reviewed are listed in the Attachment to this report. This inspection constituted one occupational radiological occurrences sample as defined in
: [[IP]] [[71151-05. b. Findings No findings of significance were identified. .7 Radiological Effluent]]
: [[TS]] [[/Offsite Dose Calculation Manual Radiological Effluent Occurrences a. Inspection Scope The inspectors sampled licensee submittals for the Radiological Effluent]]
: [[TS]] [[(]]
: [[RETS]] [[)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent Occurrences]]
: [[PI]] [[for the period from the 3rd quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the]]
: [[PI]] [[data reported during those periods,]]
: [[PI]] [[definitions and guidance contained in the]]
NEI Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 5, were used. The inspectors reviewed the licensee's issue report database and selected individual reports generated since this indicator was last reviewed to identify any potential occurrences such as unmonitored, uncontrolled, or
improperly calculated effluent releases that may have impacted offsite dose. The inspectors reviewed gaseous effluent summary data and the results of associated offsite dose calculations for selected dates between from the third quarter 2007 through the second quarter 2008, to determine if indicator results were accurately reported. The inspectors also reviewed the licensee's methods for quantifying gaseous and liquid
effluents and determining effluent dose. Additionally, the inspectors reviewed the licensee's historical
: [[10 CFR]] [[50.75(g) file and selectively reviewed the licensee's analysis for discharge pathways resulting from a spill, leak, or unexpected liquid discharge focusing on those incidents which occurred over the last few years. Documents reviewed are listed in the Attachment to this report. This inspection constituted one]]
RETS/ODCM radiological effluent occurrences sample as defined in IP 71151-05. b. Findings No findings of significance were identified.
Enclosure
: [[4OA]] [[2 Identification and Resolution of Problems (71152) Cornerstones:  Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection .1 Routine Review of items Entered Into the]]
CAP a. Scope As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensee's CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Attributes reviewed
included:  the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and that previous occurrences reviews were proper and adequate. Also, the classification, prioritization, focus, and timeliness of corrective actions were reviewed to ensure they were commensurate with safety and sufficient to prevent recurrence of the issue. Minor issues entered into the licensee's CAP as a
result of the inspectors' observations are included in the attached list of documents reviewed. These routine reviews from IP 71152 for the identification and resolution of problems did not constitute any additional inspection samples. Instead, they were considered an integral part of the inspections performed during the quarter and documented in
Section 1 of this report. b. Findings No findings of significance were identified. .2 Daily
: [[CAP]] [[Reviews a. Scope In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensee's]]
CAP. This review was accomplished through inspection of the station's daily condition report packages. These daily reviews were performed as defined in IP 71152 as part of the inspectors' daily plant status monitoring activities and, as such, did not constitute any separate inspection samples. b. Findings No findings of significance were identified.
Enclosure .3 Annual Review: Operator Workarounds (OWA) a. Scope The inspectors evaluated the licensee's implementation of their process used to identify, document, track, and resolve operational challenges. Inspection activities included, but were not limited to, a review of the cumulative effects of the OWAs on system availability and the potential for improper operation of the system, for potential impacts on multiple
systems, and on the ability of operators to respond to plant transients or accidents. The inspectors performed a review of the cumulative effects of OWAs. The documents listed in the Attachment were reviewed to accomplish the objectives of the inspection procedure. The inspectors also reviewed operator challenges, which create an obstacle to normal plant operation, rather than the more severe obstacle to safe plant operation
created by an
: [[OWA.]] [[The inspectors reviewed both current and historical operational challenge records to determine whether the licensee was identifying operator challenges at an appropriate threshold, had entered them into their]]
CAP and proposed or implemented appropriate and timely corrective actions which addressed each issue. Reviews were conducted to determine if any operator challenge could increase the possibility of an Initiating Event, if the challenge was contrary to training, required a change from long-standing operational practices, or created the potential for
inappropriate compensatory actions. Additionally, all temporary modifications were reviewed to identify any potential effect on the functionality of Mitigating Systems, impaired access to equipment, or required equipment uses for which the equipment was not designed. Daily plant and equipment status logs, degraded instrument logs, and operator aids or tools being used to compensate for material deficiencies were also
assessed to identify any potential sources of unidentified operator workarounds. In addition, interviews were conducted with equipment operators and licensed control room operators to determine if longstanding workarounds existed and had in turn been proceduralized into a part of accepted practice. This operator workarounds annual inspection review constituted one sample as defined in IP 71152. b. Findings No findings of significance were identified. .4 Annual Review: Safety-Related Procedure Changes a. Scope The inspectors reviewed a sample of approximately 100 issue reports associated with revisions to plant procedures that were associated with safety-related components or emergency operations to evaluate whether the licensee's process to identify, prioritize and resolve changes needed for those procedures was adequate. Specifically, the inspectors selected procedural changes for which the due dates were moved by more
than six months and revisions that would directly impact Emergency Operating Procedures. The inspectors evaluated the validity of extending the due date on a needed revision of a safety-related procedure and ensured the revisions were timely and commensurate with the safety significance of the issue. Additionally, the inspectors
Enclosure verified that established corrective actions by the licensee for the safety-related procedures were appropriately focused to correct the problem. b. Observations The inspectors noted that the licensee properly identified deficiencies in their procedures; however, the process for prioritizing and resolving the changes lacked some organization. Specifically, it was the responsibility of a few individuals from the
Operations and Training departments to ensure that these procedure revisions were performed in a timely manner. The inspectors noticed that there was not a formal threshold or process to establish priorities for procedures needing modification other than personal discretion and foreseen or unforeseen events. Some examples of events that influenced the establishment of due dates were refueling outages, major equipment
malfunctions and other NRC inspections. The inspectors observed that the events that influenced the priority category and original due dates for the issue reports were also used as basis for adjusting the due dates when the actions required could not be completed in time. Additionally, the inspectors noted that in most of the issue reports with postponements, no written justification was provided for deferring the completion date. The inspectors interviewed the personnel in charge of these procedure changes to gather the information on each issue and assess
whether the delays were handled in accordance with safety significance. From the sample selected, approximately 20 percent of the procedure changes required were deferred from the original due dates several times and in some cases they were pushed back by more than 6 months up to a year. The inspectors concluded that the licensee identified necessary procedural changes commensurate with safety. However, due to the workload of personnel tasked with these changes, the prioritization and execution of these procedural revisions could improve by performing a more structured significance determination and by justifying due date rescheduling to better track the program. The inspectors did not identify any issues where the resolution timeliness of the issue report compromised the safety of
plant operation. This safety related procedural changes review constituted one inspection sample as defined in
: [[IP]] [[71152. c. Findings No findings of significance were identified. 4]]
: [[OA]] [[3  Follow-Up of Events and Notices of Enforcement Discretion (71153) .1 (Closed)]]
: [[LER]] [[05000374/2008001-00, High Pressure Core Spray System Declared Inoperable Due to Failed Room Ventilation Supply Fan a. Inspection Scope  On June 11, 2008, the supply fan for the Division 3 switchgear room ventilation system (]]
VD) tripped unexpectedly. Division 3 switchgear supports the high pressure core spray (HPCS) system. High pressure core spray remained available to inject into the reactor
Enclosure vessel if needed, but was declared inoperable due to potential room heat-up with the room's ventilation failed. As
: [[HPCS]] [[is a single train system, this failure resulted in a complete loss of system function, requiring the licensee to make an eight hour notification to the]]
NRC under 10 CFR 50.72(b)(3)(v)(D). This event was also classified as a Safety System Functional Failure. The failure mechanism was identified by the licensee as a phase to ground short on the fan's motor winding. The licensee
determined the apparent cause of the motor winding failure to be a lack of a time-based refurbishment/replacement program for high duty cycle (continuously run) motors. The motor in question received periodic greasing of its bearings and quarterly vibration analysis, but no refurbishment/ replacement schedule had been established. This component was from original construction (approximately 25 years old) and vendor
environmental qualification records analyzed that this component was expected to last for the licensed lifetime of the plant (40 years). During the apparent cause investigation, the licensee identified Electric Power Research Institute (EPRI) guidance that revealed that high duty cycle motors in low power applications, such as ventilation fans, have been known to show signs of electrical degradation beginning at approximately 20 years of service. As a corrective action, the licensee established a 20 year refurbishment/replacement criteria for the supply fan in
question. The licensee performed an extent of condition review of all 480 volt motors site wide extending the 20 year criterion to all critical (safety/risk significant), high duty cycle, single train, and short duration
: [[TS]] [[shutdown time clock (less than or equal to seven days) motor driven components. This expanded the motor population to four total components (the supply and return fans associated with each units Division 3]]
: [[VD]] [[system). The inspectors' review of the]]
: [[EP]] [[]]
RI operating experience showed it to be general in nature, lacking the specificity that would reasonably cause the licensee to reevaluate previous vendor lifetime qualification data and as such the failure to establish a refurbishment/replacement criteria based on industry experience was not considered a performance deficiency. Documents reviewed in this inspection are listed in the
Attachment. This
: [[LER]] [[is closed. This event follow-up review constituted one sample as defined in Inspection Procedure 71153-05. b. Findings No findings of significance were identified. 4]]
OA5 Other Cornerstone:  Physical Protection .1 Quarterly Resident Inspector Observations of Security Personnel and Activities a. Inspection Scope During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours.
Enclosure The inspectors also reviewed a report of the results of a survey of the site security organization relative to its safety conscious work environment. The inspectors considered whether the surveys were conducted in a manner that encouraged candid and honest feedback. The results were reviewed to determine whether adequate number of staff responded to the survey. The inspectors also reviewed Exelon's self-assessment of the survey results and verified that any issues or areas for
improvement were entered into the
: [[CAP]] [[for resolution. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status review and inspection activities. b. Findings No findings of significance were identified. 4]]
: [[OA]] [[6  Management Meetings .1 Exit Meeting Summary On October 2, 2008, the inspectors presented the inspection results to Site Vice President, Mr. Daniel Enright, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary. .2 Interim Exit Meetings Interim exits were conducted for: * The results of the heat sink performance inspection with the Plant Manager, Mr.]]
: [[D.]] [[Rhoades, on July 25, 2008; and * The results of the radiation protection inspection with the Plant Manager, Mr. D. Rhodes, on August 29, 2008. The inspectors confirmed that none of the potential report input discussed was considered proprietary. 4]]
: [[OA]] [[7 Licensee-Identified Violations  None.]]
: [[ATTACH]] [[]]
: [[MENT]] [[:]]
: [[SUPPLE]] [[]]
: [[MENTAL]] [[]]
: [[INFORM]] [[]]
: [[ATION]] [[Attachment]]
: [[SUPPLE]] [[]]
: [[MENTAL]] [[]]
: [[INFORM]] [[]]
: [[ATION]] [[]]
: [[KEY]] [[]]
: [[POINTS]] [[]]
: [[OF]] [[]]
CONTACT Licensee D. Enright, Site Vice President D. Rhoades, Plant Manager J. Bashor, Site Engineering Director
: [[L.]] [[Blunk, Operations Training Manager S. Wilkinson, Chemistry Manager H. Do, Corporate Inservice Inspection Manager B. Ginter, Engineering Programs Manager F. Gogliotti, System Engineering Senior Manager]]
: [[W.]] [[Hilton, Engineering Supervisor - Mechanical/Structural K. Ihnen, Nuclear Oversight Manager A. Kochis, Inservice Inspection Engineer R. Leasure, Radiation Protection Manager S. Marik, Operations Director J. Miller,]]
NDE Level III B. Rash, Maintenance Director
: [[J.]] [[Rommel, Design Engineering Senior Manager K. Rusley, Emergency Preparedness Manager J. Shields, Inservice Inspection Program Supervisor T. Simpkin, Regulatory Assurance Manager H. Vinyard, Shift Operations Superintendent]]
: [[G.]] [[Wilhelmsen,  Design Manager J. White, Site Training Director C. Wilson, Station Security Manager D. Amezaga,]]
: [[GL]] [[89-13 Program Owner]]
: [[J.C.]] [[Feeney,]]
: [[NOS]] [[Lead Assessor]]
: [[D.]] [[Henly, Design Engineer  Nuclear Regulatory Commission K. Riemer, Chief, Reactor Projects Branch 2]]
: [[LIST]] [[]]
: [[OF]] [[]]
: [[ITEMS]] [[]]
: [[OPENED]] [[,]]
: [[CLOSED]] [[]]
: [[AND]] [[]]
: [[DISCUS]] [[SED Opened None. Closed 05000374/2008001-00]]
: [[LER]] [[High Pressure Core Spray System Declared Inoperable Due to Failed Room Ventilation Supply Fan (4]]
OA3)  Discussed None.
Attachment
: [[LIST]] [[]]
: [[OF]] [[]]
: [[DOCUME]] [[]]
: [[NTS]] [[]]
: [[REVIEW]] [[]]
: [[ED]] [[The following is a partial list of documents reviewed during the inspection. Inclusion on this list does not imply that the]]
: [[NRC]] [[inspector reviewed the documents in their entirety, but rather that selected sections or portions of the documents were evaluated as part of the overall inspection effort. Inclusion of a document on this list does not imply]]
: [[NRC]] [[acceptance of the document or any part of it, unless this is stated in the body of the inspection report. 1R04 Equipment Alignment]]
: [[PROCED]] [[]]
: [[URES]] [[Number Description or Title Date or RevisionLOP-DG-01E Unit 1 A]]
: [[DG]] [[Electrical Checklist 8/21/1997]]
: [[LOP]] [[-DG-01M Unit 1 A]]
: [[DG]] [[Mechanical Checklist 6/12/2003]]
: [[LOP]] [[-DG-04E Unit 2 A]]
: [[DG]] [[Electrical Checklist 12/17/2002]]
: [[LOP]] [[-DG-04M Unit 2 A DG Mechanical Checklist 7/24/2002]]
: [[LOP]] [[-]]
: [[DG]] [[-06M Unit 1 A]]
: [[DG]] [[Cooling System Mechanical Checklist 2/14/2008]]
: [[LOP]] [[-DG-09M Unit 2 A]]
: [[DG]] [[Cooling System Mechanical Checklist 1/7/2008]]
: [[LOP]] [[-DO-01M Unit 1 A]]
: [[DG]] [[Fuel Oil transfer System Mechanical Checklist 10/27/1997]]
: [[LOP]] [[-DO-07M Unit 2 B]]
: [[DG]] [[Fuel Oil Transfer System Mechanical Checklist 9/12/1997]]
: [[LOP]] [[-FP-01E Unit 1 Fire Protection System Electrical Checklist Rev.]]
: [[10 LOP]] [[-]]
: [[FP]] [[-01M Unit 0 Fire Protection System Mechanical Checklist Rev.]]
: [[17 LOP]] [[-]]
: [[FP]] [[-02E Unit 2 Fire Protection System Electrical Checklist Rev.]]
: [[10 LOP]] [[-]]
: [[FP]] [[-02M Unit 1 Fire Protection System Mechanical Checklist Rev.]]
: [[16 LOP]] [[-]]
: [[FP]] [[-03M Unit 2 Fire Protection System Mechanical Checklist Rev.]]
: [[14 LOP]] [[-]]
: [[LP]] [[-02E Unit]]
: [[2 LPCS]] [[System Electrical Checklist 2/27/1999]]
: [[LOP]] [[-LP-02M Unit]]
: [[2 LPCS]] [[System Mechanical Checklist 12/19/2007]]
: [[LOP]] [[-SC-02E Unit]]
: [[2 SLC]] [[System Electrical Checklist 12/15/1998]]
: [[LOP]] [[-SC-02M Unit]]
: [[2 SLC]] [[System Mechanical Checklist 12/15/1998]]
: [[CORREC]] [[TIVE]]
: [[ACTION]] [[]]
: [[PROGRA]] [[M Number Description or Title Date or Revision]]
: [[815684 NRC]] [[Walkdown Identified Concerns with]]
FP Components 9/9/2008
Attachment
: [[DRAWIN]] [[]]
: [[GS]] [[Number Description or Title Date or Revision M-140 P &]]
: [[ID]] [[Low Pressure Core Spray (]]
: [[LPCS]] [[)]]
: [[AN]] [[M-145 P &]]
: [[ID]] [[Standby Liquid Control System]]
: [[AC]] [[1R05 Fire Protection]]
: [[MISCEL]] [[LANEOUS Number Description or Title Date or Revision Fire Pre-Plan 2B1 Rx. Bldg Unit 1 elev. 720' 6" 2/2/2006 Fire Pre-Plan 2G Rx. Bldg Unit 1 elev. 710' 6" 2/2/2006 Fire Pre-Plan 2I4 Rx. Bldg Unit 1 elev. 673']]
: [[LPCS]] [[/]]
: [[RCIC]] [[Pump Cubicle 2/2/2006 Fire Pre-Plan 4F2 Aux. Bldg Unit 2 Div.]]
: [[1 ESS]] [[Switchgear Room]]
: [[EL.]] [[710' 2/2/2006 Fire Pre-Plan 7B3 710' 0"]]
: [[DG]] [[Room 2/2/2006]]
: [[LSCS]] [[-FPR, Table H3-2 Combustible Loading and Extinguishing Capability. Rev. 3  1R07 Heat Sink Performance]]
: [[PROCED]] [[]]
: [[URES]] [[Number Description or Title Date or RevisionEC364648 Replace]]
: [[0 DG]] [[Throttle Valve Rev. 1]]
: [[EC]] [[367805 Evaluation of the Standby]]
: [[DG]] [[Heat Exchanger (0, 1, and 2]]
: [[DG]] [[01A) 11/1/2007]]
: [[ER]] [[-]]
: [[AA]] [[-340]]
: [[GL]] [[89-13 Program Implementing Procedure Rev. 4]]
: [[ER]] [[-AA-340-1001]]
: [[GL]] [[89-13 Program Implementation Instructional Guidance Rev. 4]]
: [[ER]] [[-AA-340-1002  Service Water Heat Exchanger and Component Inspection Guide Rev.]]
: [[3 LOA]] [[-]]
: [[DIKE]] [[-001 Lake Dike Damage/Failure Rev.]]
: [[8 LOA]] [[-]]
: [[UHS]] [[-001 Loss of Ultimate Heat Sink Rev.]]
: [[0 LOP]] [[-]]
: [[CW]] [[-09 Circulating Water System Ice Melting Rev.]]
: [[13 LTS]] [[-200-17 Unit 1 and 2]]
: [[RHR]] [[]]
: [[HX]] [[Thermal Performance Monitoring Procedure Rev. 10]]
: [[LTS]] [[-600-23]]
: [[CSCS]] [[Cooling Water Screen Bypass Supply Line and]]
: [[CW]] [[Pump Inlet Bays Inspection Rev.]]
: [[8 OE]] [[06-001 0]]
: [[DG]] [[006 Valve Stem Separation from Disc Rev. 2]]
: [[CAP]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision 601993 2B]]
: [[RHR]] [[]]
: [[HX]] [[Did Not Pass]]
: [[VI]] [[]]
AC 3/10/2007
Attachment
: [[CAP]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision 603360 2B]]
: [[RHR]] [[]]
: [[HX]] [[As Left Inspection Not Performed by Engineering 3/13/2007 667676 Corp Engineer Review of LaSalle]]
: [[GL]] [[89-13 Surveillances and Calcs 9/4/2007 712713 Dike Maintenance Needed 12/17/2007 800212]]
: [[NRC]] [[Concern with]]
: [[ER]] [[-]]
: [[AA]] [[-340-1002 7/25/2008]]
: [[WORK]] [[]]
: [[ORDERS]] [[Number Description or Title Date or Revision355600]]
: [[DG]] [[Cooler 0A Inspection 9/3/2002 484036-01 2B]]
: [[RHR]] [[Heat Exchanger Inspection 1/5/2003]]
: [[585784 RHR]] [[Heat Exchanger Heat Transfer Test 1/13/2005 772867 Division 2]]
: [[RHR]] [[Service Water Flow Balance Test 9/25/2006 780445 Inspection of South End of]]
: [[WS]] [[Tunnel for Corbicula and Sediment 10/6/2006 785667 Perform Hydrographic Survey of]]
: [[CSC]] [[Pond per]]
: [[LTS]] [[-1000-4 1/25/2007 821559 2B]]
: [[RHR]] [[Heat Exchanger Inspection 3/4/2007 835807 Inspection of North End of]]
: [[WS]] [[Tunnel for Corbicula and Sediment 5/23/2007 848774 Clean Unit 2 A]]
: [[CW]] [[Inlet Bay 1/19/2007 848775 Clean Unit]]
: [[2 CW]] [[Inlet Bay 12/21/2006 848779 Clean Unit 1 A]]
: [[CW]] [[Inlet Bay and Bypass Line 1/5/2007 849191 Clean Unit 1 C]]
: [[CW]] [[Inlet Bay 12/14/2006 853781 Clean Unit 1 B]]
: [[CW]] [[Inlet Bay 1/24/2007]]
: [[957093 LOS]] [[-]]
: [[DG]] [[-SR5,]]
: [[0 DG]] [[Cooling Water System Flow Test 3/28/2008 1002838 Div]]
: [[II]] [[]]
: [[RHR]] [[]]
: [[WS]] [[Flow Test]]
: [[IAW]] [[]]
: [[LOS]] [[-RH-SR1 7/16/2007 1032211 Clean Unit 2 B]]
: [[CW]] [[Inlet Bay 3/13/2008]]
DRAWINGS Number Description or Title Date or Revision  Contoured Depths Ultimate Heat Sink LaSalle County Station, Sheets 1 and 2 9/21/2006 Vetip binder J-0091 RHR Heat Exchangers  S-67 Dike Sections and Details Rev. G
Attachment
: [[MISCEL]] [[]]
: [[LANEOU]] [[S Number Description or Title Date or RevisionEN-LA-402-0005 Extreme Heat Implementation Plan - LaSalle Rev.]]
: [[12 GL]] [[89-13 Program Basis Document Rev. 5]]
: [[SEAG]] [[97-000577 Evaluation of Potential Water Hammer Events Within the Core Standby Cooling System (CSCS) Equipment Cooling Water System 12/4/1997]]
: [[WR]] [[990068110]]
: [[RHR]] [[]]
: [[HX]] [[Heat Transfer Test 11/6/2000]]
: [[WR]] [[990164133]]
: [[DG]] [[Cooler 0A Inspection 2/19/2001]]
: [[CALCUL]] [[ATIONS Number Description or Title Date or Revision 97-195 Thermal Model of ComEd/LaSalle Station Unit 0, 1, and]]
: [[2 DG]] [[Jacket Water Coolers Rev. A  97-201 Thermal Model of ComEd/LaSalle Station Unit 1 and 2]]
: [[RHR]] [[Heat Exchangers]]
: [[RHR]] [[01 A&B Rev. A  L-000715 Evaluation of Potential Water Hammer Event on]]
: [[RHR]] [[]]
: [[HX]] [[]]
: [[SW]] [[(CSCS) Piping Subsystems Rev. 0  L-000718 Determination of Potential Water Hammer at the]]
: [[RHR]] [[Heat Exchanger from a Postulated]]
: [[RHRSW]] [[Void Formation Rev. 001A  L-000731 Evaluation of the]]
: [[RHR]] [[Heat Exchangers for Water Hammer Effect Rev. 2A  L-001584 Volume of the Ultimate Heat Sink Rev. 1  L-002404]]
: [[CSCS]] [[Cooling Water System "Road Map" Calculation Rev. 2b  L-002457 LaSalle County Station Ultimate Heat Sink Analysis Rev. 5a  L-002857]]
: [[RHR]] [[Heat Exchangers K Factor Sensitivity Study, 1(2)]]
: [[RHR]] [[]]
: [[01 A&B]] [[Rev. 000B Proto Power Calculation 97-201]]
: [[RHR]] [[Heat Exchanger Spec. Sheet/LaSalle Station Unit 1 and 2 Rev. A  1R11 Licensed Operator Requalification Program]]
: [[MISCEL]] [[]]
: [[LANEOU]] [[S]]
: [[ESG]] [[93 Out of the Box Training Scenario 9/2008]]
ESG 94 Out of the Box Training Scenario 9/2008
Attachment 1R12 Maintenance Effectiveness
: [[PROCED]] [[]]
: [[URES]] [[Number Description or Title Date or RevisionLGA-RD-01 Alternate Vessel Injection Using Both]]
: [[CRD]] [[Pumps Rev. 9]]
: [[CAP]] [[]]
: [[DOCUME]] [[]]
: [[NTS]] [[]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision 559645 2B]]
: [[CW]] [[]]
: [[RTS]] [[11/17/2006 569640 1C Circ Water Pump Trip 12/15/2006 570103 1A/1B]]
: [[CW]] [[Screens Running in Slow Speed with]]
: [[DP]] [[Low 12/15/2006 572545 Faulty]]
: [[TR]] [[1 Relay in 1C Circ Water Exciter Panel 12/15/2006 578017 Leak from Screen Wash Spraying Out onto Floor 1/11/2007 578368 Circ Water (]]
: [[CW]] [[) has met its maint. rule reliability criteria 1/12/2007 589768 Unexplained U1 and U2]]
: [[CW]] [[Flow Changes 2/9/2007 608413 U-1 C]]
CW Pump tripped on Start 3/24/2007
613901 L2R11
: [[LL]] [[to Apply to L1R12 for the]]
: [[CW]] [[System 4/6/2007 619180 Unit-1]]
: [[CW]] [[Exceeds Maint Rule Reliability Target 4/19/2007 620755 Foreign Material Found Lodged in Pump Impeller 4/23/2007 623904 Traveling Screen Nozzle Plugged 5/1/2007 626910 Interim Corrective Actions for]]
: [[CW]] [[Pump Motor Trips 5/18/2007]]
: [[643422 M.R.]] [[(A)(1) Determination Paper Work Not Completed on Time 6/22/2007 734960 1C11-F004]]
: [[CRD]] [[Drive Water]]
: [[PCV]] [[Bypass Could Not be Opened 2/12/2008 740876 1A Circ. Water Pump Slip Guard Relay Tripped During Start 2/25/2008 777914 Received 'Circ Wtr Pmp Dsch Vlv fail to open alarm' 5/21/2008 797547 Trip of 1A Circ Water Pump 7/17/2008 800641 1]]
: [[CW]] [[093A Pump Leak 7/27/2008]]
: [[808472 VQ]] [[Inerting Line badly Corroded and Needs Repainting 8/19/2008 808504 Rebuilt Check Valve is Non-Conformance 8/19/2008 809238 Circ Water]]
MRFF status 8/20/2008 809641 Work on CW Pumps was moved out several times 8/21/2008
Attachment
: [[MISCEL]] [[]]
: [[LANEOU]] [[S Number Description or Title Date or Revision]]
: [[BWR]] [[Delphi Form  Maintenance Rule Expert Panel Meeting Agenda 1/31/2008  Maintenance Rule Expert Panel Meeting Agenda 5/15/2008  Maintenance Rule Expert Panel Meeting Agenda 5/17/2007  Maintenance rule Functional Failure Evaluation 3/13/2008  Maintenance Rule Performance Criteria]]
RD-02:  Functional Failure includes failure of a CRD pump or failure of the flow path
specified in
: [[LGA]] [[-]]
: [[RD]] [[-01 5/8/2008  Maintenance Rule Scoping for]]
: [[RD]] [[-02 5/8/2008  Performance Criteria - Unavailability Criteria -]]
: [[CW]] [[8/11/2008  Performance Monitoring - Reliability]]
: [[CW]] [[-01 Unit 1 8/2006 - 8/2008  Performance Monitoring - Reliability]]
: [[CW]] [[-01 Unit 2 8/2006 - 8/2008  Performance Monitoring - Reliability Details]]
: [[CW]] [[Unit 1 8/2006 - 8/2008  Performance Monitoring - Unavailability]]
: [[CW]] [[-01 Unit 1 8/2006 - 8/2008  Performance Monitoring - Unavailability]]
: [[CW]] [[-01 Unit 2 8/2006 - 8/2008  Performance Monitoring Summary -]]
: [[CW]] [[Reliability  Scoping and Risk Significance - Scoping -]]
: [[CW]] [[8/11/2008  Scoping/Risk Significance Detailed Report:]]
: [[CW]] [[Circulating Water 4/28/2005]]
: [[WORK]] [[]]
: [[REQUES]] [[TS Number Description or Title Date or Revision 263217 1C11-F004]]
: [[CRD]] [[Drive Water]]
PCV Bypass Could Not be Opened 2/14/2008
Attachment 1R13  Maintenance Risk Assessments and Emergent Work Control
: [[PROCED]] [[]]
: [[URES]] [[Number Description or Title Date or RevisionLOP-EH-04 Shifting Pumps and Pressure Adjustment in the Electro Hydraulic Control System (EHC) Rev.]]
: [[9 LOP]] [[-]]
: [[EH]] [[-08 Changing]]
: [[EHC]] [[Fuller's Earth, Pump Discharge Duplex, and Back-up Filters Rev. 26]]
: [[WORK]] [[]]
: [[DOCUME]] [[]]
: [[NTS]] [[Number Description or Title Date or Revision]]
: [[WO]] [[1125757-0-2 M116 Main Steam - Interim Changeout of 2]]
: [[EH]] [[02MB, 2B]]
: [[EHC]] [[Duplex Filter]]
: [[WO]] [[1137641-01 /]]
: [[EC]] [[368841 Bypass the Unit 2]]
: [[EHC]] [[Low Hydraulic Pressure Trip Signal at]]
: [[2PA]] [[01]]
: [[JX]] [[Rev. 0]]
: [[CAP]] [[]]
: [[DOCUME]] [[NTS Number Description or Title Date or Revision 810538 Through Wall Leak in Line]]
: [[0WS]] [[09]]
: [[AB]] [[8/25/2008 811599 Extent of Condition of the Nonsafety]]
: [[WS]] [[Pipe Leak at the]]
: [[LSH]] [[8/27/2008 814647 Water Leak]]
: [[FRM]] [[Cable Troughs into Concrete Cut Out for]]
: [[WS]] [[]]
: [[PP]] [[9/5/2008]]
: [[DRAWIN]] [[GS Number Description or Title Date or Revision M-68 P &]]
: [[ID]] [[Service Water System]]
: [[AF]] [[]]
: [[CALCUL]] [[]]
: [[ATIONS]] [[Number Description or Title Date or Revision]]
: [[EC]] [[368841]]
: [[MR]] [[90(a)(4) Technical Evaluation of W/O 10913780 in Support of Maintenance of the 2A]]
: [[EHC]] [[Pump to Allow the Bypass of the 2B]]
EHC Pump Trip During Swap Over from the 2A EHC Pump Rev. 0
Attachment
: [[MISCEL]] [[]]
: [[LANEOU]] [[S Number Description or Title Date or Revision  Plant Status:  LaSalle Plant Conditions 7/9/2008  Personnel Safety Work Requests - Work Orders Status  7/8/2008  1R15 Operability Evaluations]]
: [[PROCED]] [[]]
: [[URES]] [[Number Description or Title Date or RevisionLOP-RH-01 Filling and Venting the]]
: [[RHR]] [[System Rev. 40]]
: [[OP]] [[-AA-108-115 Operability Evaluation]]
: [[OE]] [[08-003 Rev. 6]]
: [[TRM]] [[3.7.G-1 Plant Systems:  Area Temperature Monitoring Rev.]]
: [[1 LOS]] [[-]]
: [[AA]] [[-S101 Unit 1 Shiftly Surveillance Rev. 50]]
: [[CAP]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision 765918]]
: [[1TE]] [[-]]
: [[VP]] [[079 Temp. Indication High out of]]
: [[LOS]] [[-]]
: [[AA]] [[-S101 Band. 4/22/2008 782609]]
: [[1TE]] [[-]]
: [[VP]] [[079 Approaching]]
: [[TRM]] [[Limit 6/4/2008 790001 1]]
: [[TE]] [[-VP079 Drywell Temp Continues to Rise 6/25/2008]]
: [[792505 DIV]] [[3]]
: [[DC]] [[Issues Found During Key Calc Reviews 7/1/2008 795015 Beneath Reactor Vessel Temp Exceeds]]
: [[TRM]] [[Limit 7/10/2008 795018 Discrepancy Noticed with]]
: [[TRM]] [[3.7.G Condition B Versus Bases 7/10/2008]]
: [[798182 RRC]] [[]]
: [[GL]] [[2008-01 Gas Intrusion Field Activities (1E12-F340) 7/18/2008]]
: [[811220 NRC]] [[]]
: [[GL]] [[2008-01 Tech Evals - Fleet Wide Gaps 8/25/2008 813453 Need Confirmatory]]
: [[UT]] [[of Unit 1]]
: [[HPCS]] [[System High Point 9/3/2008 816204 Air Pocket Detected in High Point of]]
: [[HP]] [[]]
CS System Piping 9/10/2008 817402 High Lake Level 9/13/2008 817934 High River Level, Lake Blowdown Flow Control Valve Submerged 9/15/2008 819095 Lessons Learned from High Lake Level during Heavy Rain 9/17/2008 819602 Lake Blowdown Valve Data during River Flood 9/18/2008
Attachment
: [[CALCUL]] [[]]
: [[ATIONS]] [[Number Description or Title Date or Revision 4266/19AN77 (Sargent & Lundy) Calc. for Motor Control Center (MCC) Setting for Motor Operated Valve (MOV) Rev.]]
: [[2 EC]] [[371858]]
: [[TOL]] [[Relay Setting Change for]]
: [[MOV]] [[1E12-F004C 8/21/2008]]
: [[EC]] [[371494 Potential for Trapped Air in the]]
: [[HPCS]] [[System Rev. 9]]
: [[EC]] [[371495 Potential for Trapped Air in the]]
: [[LPCS]] [[System Rev. 9]]
: [[EC]] [[371496 Potential for Trapped Air in the]]
: [[RHR]] [["A" System Rev. 9]]
: [[EC]] [[371497 Potential for Trapped Air in the]]
: [[RHR]] [["B" System Rev. 9]]
: [[EC]] [[371498 Potential for Trapped Air in the]]
: [[RHR]] [["C" System Rev. 9]]
: [[EC]] [[371571 Potential for Trapped Air in Portions of]]
: [[RHR]] [["A" & "B" Systems Rev. 9]]
: [[OPERAB]] [[ILITY]]
: [[EVALUA]] [[]]
: [[TION]] [[Number Description or Title Date or Revision 97040 Flooding of Turbine Building Due to Overflow of Condenser Pit with Lake Level Greater than 701' Elevation 7/30/1997 97041 Effects of Lake Level Greater than 701' Elevation on External Plant Structures 3/12/1997 97042 Effects of Flooding in Unit 1 Division]]
: [[2 CSCS]] [[Pump Room on Unit 1 Division 1]]
: [[CSCS]] [[Pump Room where Lake Level is Greater than 701' Elevation 3/13/1997]]
: [[DRAWIN]] [[]]
: [[GS]] [[Number Description or Title Date or Revision]]
: [[ISI]] [[-]]
: [[RH]] [[-1002 Inservice Inspection (ISI) Isometric]]
: [[RHR]] [[System Rev. A]]
: [[ISI]] [[-RH-1005]]
: [[ISI]] [[Isometric]]
: [[RHR]] [[System Rev. A]]
: [[ISI]] [[-]]
: [[RH]] [[-1006]]
: [[ISI]] [[Isometric]]
: [[RHR]] [[System Rev. A]]
: [[MISCEL]] [[]]
: [[LANEOU]] [[S Number Description or Title Date or Revision]]
: [[ER]] [[-]]
AA-600-1045 Risk Assessments of Missed or Deficient Rev. 2
Attachment
: [[MISCEL]] [[]]
LANEOUS Number Description or Title Date or Revision Surveillances GL 2008-01 Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and
Containment Spray Systems 1/11/2008
: [[LS]] [[-]]
SURV-01 Missed Surveillance Risk Assessment for the Units 1 and 2 Division 3 (HPCS) Battery 
(IR 792505) Rev. 0  Cooling Lake Level Trend Chart 9/14/08 - 9/15/08  1R18 Plant Modifications
: [[PROCED]] [[]]
: [[URES]] [[Number Description or Title Date or Revision88629/L92050 Vol.J-0617 Operating Instruction for Carrier Centrifugal Refrigeration Machines 3/17/1981]]
: [[DRAWIN]] [[]]
: [[GS]] [[Number Description or Title Date or Revision 1E-1-4081AN Schematic Diagram Primary Containment]]
: [[VD]] [["]]
: [[VP]] [[" Water Chiller 1A Part 12 3/19/1999 1E-1-4081AN Schematic Diagram Primary Containment]]
: [[VD]] [["]]
: [[VP]] [[" Water Chiller 1A Part 13 2/23/2001 1E-1-4081AQ Schematic Diagram Primary Containment]]
: [[VD]] [["]]
: [[VP]] [[" Water Chiller 1B Part 15 2/23/2001]]
: [[DRAWIN]] [[]]
: [[GS]] [[Number Description or Title Date or Revision]]
: [[EC]] [[371742 Jumper]]
: [[VP]] [[Chillers Defective Chill Water Outlet Switches Rev. 0  1R19 Post-Maintenance Testing]]
: [[PROCED]] [[]]
: [[URES]] [[Number Description or Title Date or RevisionLOS-DG-M1]]
: [[0 DG]] [[Fast Start, Attachment 0-Fast 10/24/2008]]
: [[LOS]] [[-DG-Q3 1B(2B)]]
: [[DG]] [[Auxiliaries Inservice Test; Attachments B3 and B4 Rev. 51]]
LOS-PC-Q1 Primary Containment Isolation Valves Rev. 40
Attachment
: [[PROCED]] [[]]
: [[URES]] [[Number Description or Title Date or RevisionOperability Test and]]
: [[ISI]] [[]]
: [[LOS]] [[-RH-Q1]]
: [[RHR]] [[(]]
: [[LPCI]] [[) and]]
: [[RHR]] [[Service Water Pump and Valve Inservice Test for Modes 1,2,3,4 and 5 Rev. 67]]
: [[LOS]] [[-RH-Q2]]
: [[RHR]] [[(]]
: [[LPCI]] [[) and]]
: [[RHR]] [[Service Water Valve Inservice Test for Operating, Startup and Hot Shutdown Conditions Rev. 41]]
: [[CAP]] [[]]
: [[DOCUME]] [[]]
: [[NTS]] [[]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision 605457 2B]]
: [[DG]] [[Air Pressure Alarm 3/17/2007 616025 Low Air Pressure Alarm 2E22-N506 4/11/2007 802717 1]]
: [[RF]] [[013 Close Time > Required Action Range 8/1/2008 803468 Request]]
: [[CCA]] [[Be Performed on Configuration Control Events 8/4/2008 808710 1C]]
: [[RHR]] [[Suction Valve Tripped Thermal Overloads 8/19/2008 808859 1C]]
: [[RHR]] [[Suction Valve tripped Thermal Overload 8/20/2008]]
: [[WORK]] [[]]
: [[ORDERS]] [[Number Description or Title Date or Revision 545611 Contingency for]]
: [[DWFD]] [[Loop Instruments 8/1/2008]]
: [[MISCEL]] [[]]
: [[LANEOU]] [[S Number Description or Title Date or Revision]]
: [[ASCO]] [[Internal Pilot Operated Solenoid Valves Technical Specification  1R22 Surveillance Testing]]
: [[PROCED]] [[URES Number Description or Title Date or RevisionLOS-AA-S101 Unit 1 Shiftly Surveillance Rev.]]
: [[50 LOS]] [[-]]
: [[AA]] [[-S201 Unit 2 Shiftly Surveillance Rev.]]
: [[58 LOS]] [[-]]
: [[RH]] [[-Q1]]
: [[RHR]] [[(]]
LPCI) and RHR Service Water Pump and Valve Inservice Test for Modes 1, 2, 3, 4 Rev. 67
Attachment
: [[PROCED]] [[]]
: [[URES]] [[Number Description or Title Date or Revisionand]]
: [[5 LOS]] [[-]]
: [[RH]] [[-Q1 Tech Spec Surveillance:  2B]]
: [[RHR]] [[Att. 2B 7/2/2008]]
LOS-RI-Q5 Reactor Core Isolation Cooling (RCIC) System Pump Operability, Valve Inservice tests in Modes 1,2,3 and Cold Quick Start;
1A Rev.
: [[28 LOS]] [[-]]
: [[SC]] [[-Q1 2B]]
: [[SLC]] [[Pump Qtrly Att. 2B 9/5/2008]]
: [[LOS]] [[-SC-Q1]]
: [[SLC]] [[Pump Operability/Inservice Test and Explosive Valve Continuity Check 8/5/2008]]
: [[LOS]] [[-VC-SR1 Control Room and Auxiliary Electric Equipment Room]]
: [[HVAC]] [[Pressurization Surveillance 8/12/2008]]
: [[CAP]] [[]]
: [[DOCUME]] [[]]
: [[NTS]] [[]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision]]
: [[745140 SLC]] [[Test Tank (2C41-A002) Requires Flushing]]
: [[IAW]] [[]]
: [[LOP]] [[-]]
: [[SC]] [[-07 3/5/2008 816217 Design Eng to Eval Max opening Size in]]
: [[CRE]] [[after]]
: [[DP]] [[Test 9/15/2008]]
: [[WORK]] [[]]
: [[ORDERS]] [[Number Description or Title Date or Revision 1017479 "A"]]
: [[VC]] [[System]]
: [[DP]] [[Test 9/4/2008 1017480 "B"]]
: [[VC]] [[System]]
: [[DP]] [[Test 9/4/2008]]
: [[1EP]] [[6 Drill Evaluation]]
: [[MISCEL]] [[LANEOUS]]
: [[ESG]] [[93 Out of the Box Training Scenario 9/2008]]
ESG 94 Out of the Box Training Scenario 9/2008
Attachment 20S1 Access Control to Radiologically Significant Areas
: [[CAP]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision758197 L1R12 Steam Affected Dose 8.579 Person-Rem Over Estimate 4/2/2008 785091 Operator Is Contaminated During Hanging of Clearance Order 6/10/2008 786202 Need to Lower Dose Rates in Unit 2 Reactor Building 673 and 694 North 6/13/2008 793324 Limiting Use of Danger Locked High Radiation Area Master Keys 7/3/2008 804553 Personnel Contamination Discovered at Radiologically Restricted Area Exit 8/6/2008 806465 Procedure Guidance Does Not Conform with]]
: [[ODCM]] [[Section 2.3 8/12/2008 907817 High Radiation Area Found While Performing Routine Survey 8/16/2008]]
: [[MISCEL]] [[LANEOUS Number Description or Title Date or RevisionLS-AA-126-1001 Access Control to Radiologically Significant Areas and]]
: [[ALARA]] [[Planning and Controls Self-Assessment Report 1/30/2008]]
: [[NF]] [[-AA-390  Spent Fuel Pool Material Control Rev. 2  20S2]]
: [[ALARA]] [[Planning and Controls]]
: [[PROCED]] [[URES Number Description or Title Date or RevisionRP-AA-270 Prenatal Radiation Exposure Rev.]]
: [[3 RP]] [[-]]
: [[AA]] [[-401]]
: [[ALA]] [[]]
RA Post-Job review L1R12 Safety Relief Valve Activities 2/23/2008  L1R12 Refueling Outage Report 2/2008
Attachment
: [[4OA]] [[1 Performance Indicator Verification]]
: [[PROCED]] [[URES Number Description or Title Date or RevisionNEI 99-02 Performance Indicators Rev. 5]]
: [[CAP]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision 727701 Turbine Control Valve]]
: [[1 LVDT]] [[1 Connection Degraded 1/28/2008 744657 14A Heater Normal Drain Controller 3/4/2008 768445 Received]]
: [[EHC]] [[Minor Alarm]]
: [[CV]] [[#4]]
: [[LVDT]] [[Fault 4/28/2008]]
: [[MISCEL]] [[]]
: [[LANEOU]] [[S Number Description or Title Date or Revision]]
: [[LS]] [[-]]
: [[AA]] [[-2090 Monthly Data Elements for]]
: [[NRC]] [[Reactor Coolant System (]]
: [[RCS]] [[) Specific Activity Rev.]]
: [[4 LS]] [[-]]
: [[AA]] [[-2030 Monthly Data Elements for]]
: [[NRC]] [[Unplanned Power Changes per 7000 Critical Hours Rev. 5]]
: [[LS]] [[-AA-2010 Monthly Data Elements for]]
: [[NRC]] [[/]]
: [[WANO]] [[Unit/Reactor Shutdown Occurrences Rev. 5 1Q/2008]]
: [[PI]] [[1Q/2008 Performance Indicators - La Salle 1 7/22/2008 1Q/2008]]
: [[PI]] [[1Q/2008 Performance Indicators - La Salle 2 7/22/2008]]
: [[LS]] [[-]]
: [[AA]] [[-126-1005 Reactor Coolant System Activity Check-In Self-Assessment Report 3/5/2008]]
: [[LS]] [[-]]
: [[AA]] [[-2140 Monthly Data Elements for Occupational Exposure Control Effectiveness Rev.]]
: [[4 LS]] [[-]]
: [[AA]] [[-2150 Monthly Data Elements for]]
: [[RETS]] [[/]]
ODCM Radiological Effluent Occurrences Rev. 5
Attachment
: [[4OA]] [[2 Identification and Resolution of Problems]]
: [[PROCED]] [[URES Number Description or Title Date or RevisionLGA-RI-101 Unit 1 Alternate Vessel Injection using]]
: [[RCIC]] [[including Defeat of]]
: [[RCIC]] [[Isolations Rev.]]
: [[3 LGA]] [[-]]
: [[RI]] [[-103 Unit]]
: [[1 RPV]] [[Injection using]]
: [[RCIC]] [[when Loss of]]
: [[DC]] [[is Imminent or has Occurred Rev. 1]]
: [[LOA]] [[-AP-101 Unit 1,]]
: [[AC]] [[Power System Abnormal Rev. 30]]
: [[LOP]] [[-CM-02 Startup, Operation and Shutdown of Post-LOCA Primary Containment Atmosphere Hydrogen and Oxygen Monitoring System Rev.]]
: [[27 LOP]] [[-]]
: [[GC]] [[-02 Adding Makeup Water to Generator Stator Cooling System (GC) Rev.]]
: [[11 LOP]] [[-]]
: [[RT]] [[-05 Reactor Water Cleanup System Filter/Demineralizer Backwash Rev.]]
: [[38 OP]] [[-]]
: [[AA]] [[-102-103 Operator Work-Around Program Rev. 1]]
: [[CAP]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision 517613 - Assign. 9 Revise procedures to support Riverbend Seismic]]
: [[OPEX]] [[9/21/2006 517613 - Assign. 17 Revise Isolation Interlock Defeat Methodology in]]
: [[LGA]] [[s 5/18/2007 517613 - Assign. 33 Implement]]
: [[OP]] [[-]]
: [[AA]] [[-103-105 and Rev. 24 of]]
: [[LOP]] [[-]]
: [[AA]] [[-04. 4/6/2007 517613 - Assign. 36 Revise]]
: [[LGA]] [[-]]
: [[HD]] [[-101/201 for]]
: [[PRA]] [[6/1/2007 517613 - Assign. 39 Revise Post Op Auth Procedures for]]
: [[EC]] [[357861 Procedures]]
: [[LOA]] [[-]]
: [[IA]] [[-201,]]
: [[LOA]] [[-]]
: [[OG]] [[-201,]]
: [[LOP]] [[-]]
: [[HW]] [[-03M and]]
: [[LOP]] [[-]]
: [[HW]] [[-04M 6/22/2007 517613 - Assign. 40 Revise post Op Auth Procedures for]]
: [[EC]] [[364867 6/29/2007 517613 - Assign. 43 Revise procedures for Post]]
: [[LOCA]] [[H2 Indication Fix]]
: [[EC]] [[365109 will replace the recorder scales for H2 recorder or put in new recorders 8/10/2007 517613 - Assign. 44]]
: [[LOA]] [[-FP-001 revise and approve for distribution. 5/10/2007 517613 - Assign. 48 Revise]]
: [[LOP]] [[-]]
: [[VE]] [[-01 for]]
: [[EC]] [[365986 9/7/2007 517613 - Assign. 65 Revise as necessary the]]
: [[EOP]] [[Support Procs and]]
: [[EOP]] [[Flowcharts for Calc L-003317 3/14/2008 650784]]
: [[CDBI]] [[- Manual Suction Swap in]]
: [[RCIC]] [[Black Start Too Late 7/12/2007 608495 Maintenance Rework-]]
GC Vacuum Breaker 3/24/2007
Attachment
: [[CAP]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision Leaking Past Seat 608495 - Assign. 2 To Evaluate and Implement as appropriate actions to address the condition prior to a refueling outage 4/26/2007 718764 B/W won't Advance to to]]
: [[LVL]] [[Switch or Vacuum in Vessel 1/7/2008 774168 Long term degraded condition no resolution 5/10/2008 779879 Unit 1 "A"]]
: [[OG]] [[Recombiner Inlet Temperature Reads Upscale 5/27/2008 795493 Chronic Repeat Event-VL Compressor Trips on High Oil Temp 7/11/2008 812327 Can't Maintain Corrected Flow when Switch in Auto Position 8/29/2008]]
: [[814201 FP]] [[]]
: [[FASA]] [[Entry Conditions for Safe Shutdown Procedures 9/4/2008]]
: [[814237 FP]] [[]]
: [[FASA]] [[]]
: [[IR]] [[364029 - Required Action Not Completed 2/7/2008]]
: [[MISCEL]] [[LANEOUS Number Description or Title Date or Revision  Operator Workarounds and Challenges 8/4/2008]]
: [[4OA]] [[3  Follow-Up of Events and Notices of Enforcement Discretion]]
: [[PROCED]] [[URES Number Description or Title Date or Revision]]
: [[LER]] [[05000374/2008001-00]]
: [[HPCS]] [[System Declared Inoperable Due to Failed Room Ventilation Supply Fan 8/8/2008]]
: [[MA]] [[-]]
: [[AA]] [[-716-210 Performance Centered Maintenance Process Rev.]]
: [[7 MA]] [[-]]
: [[AA]] [[-716-210-1002 Exelon Motor Maintenance Logic Tree Rev. 3]]
: [[CAP]] [[]]
: [[DOCUME]] [[NTS]]
: [[REVIEW]] [[]]
: [[ED]] [[Number Description or Title Date or Revision]]
: [[AR]] [[785154-15-02 Licensee Extent of Condition review for Applicable 480]]
: [[VAC]] [[Motors 9/5/2008 785154]]
: [[2VD]] [[05C Tripped 6/11/2008 785154 Assign. 3]]
EACE - Investigate 2VD05C tripped 7/10/2008
Attachment
: [[MAIN]] [[]]
: [[CONTRO]] [[L]]
: [[ROOM]] [[]]
: [[OPERAT]] [[OR]]
: [[LOGS]] [[Number Description or Title Date or Revision 6/11/2008 6:21:24 A.M. Rolled Forward Entry 6/11/2008]]
: [[VENDOR]] [[]]
: [[MANUAL]] [[Number Description or Title Date or Revision  Baldor-Reliance Integral Horsepower]]
: [[AC]] [[Induction Motors Installation & Operating Manual 2/2007]]
: [[EPRI]] [[1003095 Electric Motor Tiered Maintenance Program 8/2002]]
: [[EPRI]] [[]]
: [[NP]] [[-7502s Electric Motor Predictive and Preventive Maintenance Guide 7/1992]]
: [[MISCEL]] [[LANEOUS Number Description or Title Date or Revision]]
: [[EN]] [[#44284 Reactor Plant Event Notification Worksheet 6/11/2008]]
: [[EPRI]] [[1000898 Random Wound Motor Failure Investigation Technical Evaluation 12/2000]]
: [[EQ]] [[-]]
: [[LS]] [[067 Reliance Electric Company Ventilation Fan Motors Justification and Analysis Rev. 15 Figure 128-2]]
: [[HPCS]] [[Switchgear and Pump Room ventilation System 2/2003]]
FOR ZVD05C Work History Report by System 9/17/2008
Attachment
: [[LIST]] [[]]
: [[OF]] [[]]
: [[ACRONY]] [[]]
: [[MS]] [[]]
: [[USED]] [[]]
: [[ALARA]] [[As-Low-As-Is-Reasonably-Achievable]]
: [[CAP]] [[Corrective Action Program]]
: [[CFR]] [[Code of Federal Regulations]]
: [[CRD]] [[Control Rod Drive]]
: [[CSCS]] [[Core Standby Cooling System]]
: [[CW]] [[Circulating Water]]
: [[DG]] [[Diesel Generator]]
: [[EHC]] [[Electro-Hydraulic Control]]
: [[EPRI]] [[Electric Power Research Institute]]
: [[HP]] [[]]
: [[CS]] [[High Pressure Core Spray]]
: [[IP]] [[Inspection Procedure]]
: [[ISI]] [[Inservice Inspection]]
: [[LOCA]] [[Loss of Coolant Accident]]
: [[LPCI]] [[Low Pressure Coolant Injection]]
: [[LPCS]] [[Low Pressure Core Spray]]
: [[MOV]] [[Motor-Operated Valve]]
: [[MR]] [[]]
: [[FF]] [[Maintenance Rule Functional Failure]]
: [[NEI]] [[Nuclear Energy Institute]]
: [[NRC]] [[]]
: [[U.S.]] [[Nuclear Regulatory Commission]]
: [[ODCM]] [[Offsite Dose Calculation Manual]]
: [[OWA]] [[Operator Workaround]]
: [[PARS]] [[Publicly Available Records]]
: [[PI]] [[Performance Indicator]]
: [[PMT]] [[Post-Maintenance Testing]]
: [[RCIC]] [[Reactor Core Isolation Cooling]]
: [[RCS]] [[Reactor Coolant System]]
: [[RE]] [[]]
: [[TS]] [[Radiological Effluent Technical Specifications]]
: [[RHR]] [[Residual Heat Removal]]
: [[RHRSW]] [[Residual Heat Removal Service Water]]
: [[RWP]] [[Radiation Work Permit]]
: [[SLC]] [[Standby Liquid Control TS Technical Specification]]
: [[UFSAR]] [[Updated Final Safety Analysis Report]]
: [[USAR]] [[Updated Safety Analysis Report]]
: [[UHS]] [[Ultimate Heat Sink]]
VD Ventilation System VP Containment Ventilation
: [[WO]] [[Work Order]]
}}
}}

Latest revision as of 14:28, 14 January 2025

IR 05000373-08-004, 05000374-08-004; Exelon Generation Company, LLC; 7/01/2008 - 9/30/2008; LaSalle County Station, Units 1 & 2, Routine Integrated Report
ML083100251
Person / Time
Site: LaSalle  Constellation icon.png
Issue date: 11/04/2008
From: Kenneth Riemer
NRC/RGN-III/DRP/B2
To: Pardee C
AmerGen Energy Co, Exelon Nuclear
References
IR-08-004
Download: ML083100251 (46)


Text

November 4, 2008

SUBJECT:

LASALLE COUNTY STATION, UNITS 1 AND 2 NRC INTEGRATED INSPECTION REPORT 05000373/2008004; 05000374/2008004

Dear Mr. Pardee:

On September 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an integrated inspection at your LaSalle County Station, Units 1 and 2. The enclosed report documents the results of this inspection, which were discussed on October 2, 2008, with Site Vice President, Mr. Daniel Enright, and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.

Based on the results of this inspection, no NRC-identified or self-revealed findings of safety significance were identified. There were no findings involving a violation of NRC requirements.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kenneth Riemer, Chief Branch 2 Division of Reactor Projects Docket Nos. 50-373; 50-374 License Nos. NPF-11; NPF-18

Enclosure:

Inspection Report 05000373/2008004; 05000374/2008004 w/Attachment: Supplemental Information cc w/encl:

Site Vice President - LaSalle County Station

Plant Manager - LaSalle County Station

Regulatory Assurance Manager - LaSalle County Station

Chief Operating Officer and Senior Vice President

Senior Vice President - Midwest Operations

Senior Vice President - Operations Support

Vice President - Licensing and Regulatory Affairs

Director - Licensing and Regulatory Affairs

Manager Licensing - Braidwood, Byron and LaSalle

Associate General Counsel

Document Control Desk - Licensing

Assistant Attorney General J. Klinger, State Liaison Officer, Illinois Emergency Management Agency

Chairman, Illinois Commerce Commission

SUMMARY OF FINDINGS

IR 05000373/2008004, 05000374/2008004; 7/01/2008 - 9/30/2008; LaSalle County Station,

Units 1 & 2; routine integrated report.

The inspection was conducted by U.S. Nuclear Regulatory Commission (NRC) resident inspectors and regional inspectors. The report covers a three-month period of resident inspection, and announced inspection in the areas of health physics, heat sink performance, and diesel generator performance testing. No findings of significance were identified. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

Inspector-Identified and Self-Revealed Findings No findings of significance were identified.

Licensee-Identified Violations

No violations of significance were identified.

REPORT DETAILS

Summary of Plant Status

Unit 1 The unit began the inspection period operating at full power. On July 20, 2008, the unit was reduced to 82 percent for motor driven reactor feed pump and main turbine valve surveillance testing. The unit returned to full power that same day. On September 6, 2008, power was reduced to approximately 66 percent to perform control rod sequence exchange and scram time testing. Operation at full power resumed on September 7, 2008. On September 28, 2008, the unit was shutdown to perform repairs of a hydrogen leak on the main generator housing. The unit remained in mode 3 (hot shutdown) for the rest of the inspection period.

Unit 2 The unit began the inspection period operating at full power. On July 27, 2008, power was reduced to approximately 62 percent for channel distortion testing of all the interior rods. The unit was returned to full power that same day. On August 30, 2008, the unit commenced a reduction in power to 53 percent for control rod sequence exchange and feedwater pump turbine surveillances. The unit was returned to full power on August 31, 2008, where it remained until September 26, 2008. At this time, power was reduced to 55 percent for power suppression testing, control rod SCRAM time testing and channel distortion testing. Full power was restored on September 29, 2008, and the unit remained operating at or near full power for the rest of the inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency Preparedness

1R04 Equipment Alignment

.1 Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • 1A and 2A diesel generators (DG) and support systems with the 0 DG out of service.

The inspectors selected these systems based on their risk significance relative to the Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted to identify any discrepancies that could impact the function of the system, and, therefore, potentially increase risk. The inspectors reviewed applicable operating procedures, system diagrams, Updated Final Safety Analysis Report (UFSAR), Technical Specification (TS) requirements, outstanding work orders, condition reports, and the impact of ongoing work activities on redundant trains of equipment in order to identify conditions that could have rendered the systems incapable of performing their intended functions. The inspectors also walked down accessible portions of the systems to verify system components and support equipment were aligned correctly and operable. The inspectors examined the material condition of the components and observed operating parameters of equipment to verify that there were no obvious deficiencies. The inspectors also verified that the licensee had properly identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers and entered them into the corrective action program (CAP) with the appropriate significance characterization. Documents reviewed are listed in the Attachment.

These activities constituted three partial system walkdown samples as defined in Inspection Procedure (IP) 71111.04-05.

b. Findings

No findings of significance were identified.

.2 Semi-Annual Complete System Walkdown

a. Inspection Scope

On August 27 through August 29, 2008, the inspectors performed a complete system alignment inspection of the fire protection system to verify the functional capability of the system. This system was selected because it was considered risk-significant in the licensees probabilistic risk assessment. The inspectors walked down the system to review mechanical and electrical equipment line ups, electrical power availability, system pressure and temperature indications, as appropriate, component labeling, component lubrication, component and equipment cooling, hangers and supports, operability of support systems, and to ensure that ancillary equipment or debris did not interfere with equipment operation. A review of a sample of past and outstanding work orders (WOs)was performed to determine whether any deficiencies significantly affected the system function. In addition, the inspectors reviewed the CAP database to ensure that system equipment alignment problems were being identified and appropriately resolved.

Documents reviewed are listed in the Attachment to this report.

These activities constituted one complete system walkdown sample as defined in IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

.1 Routine Resident Inspector Tours

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability, accessibility, and the condition of firefighting equipment in the following risk-significant plant areas:

  • Fire Zone 7B3 0 DG Room;
  • Fire Zone 4F2 Unit 2 Division 1 switchgear;
  • Fire Zone 2G Unit 1 reactor building 710;
  • Fire Zone 2B1 Unit 1 reactor building 820.

The inspectors reviewed areas to assess if the licensee had implemented a fire protection program that adequately controlled combustibles and ignition sources within the plant, effectively maintained fire detection and suppression capability, maintained passive fire protection features in good material condition, and had implemented adequate compensatory measures for out-of-service, degraded or inoperable fire protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk as documented in the plants Individual Plant Examination of External Events with later additional insights, their potential to impact equipment which could initiate or mitigate a plant transient, or their impact on the plants ability to respond to a security event. Using the documents listed in the Attachment, the inspectors verified that fire hoses and extinguishers were in their designated locations and available for immediate use; that fire detectors and sprinklers were unobstructed, that transient material loading was within the analyzed limits; and fire doors, dampers, and penetration seals appeared to be in satisfactory condition. The inspectors also verified that minor issues identified during the inspection were entered into the licensees CAP. Documents reviewed are listed in the Attachment to this report.

These activities constituted five quarterly fire protection inspection samples as defined in IP 71111.05-05.

b. Findings

No findings of significance were identified.

1R07 Heat Sink Performance

.1 Triennial Review of Heat Sink Performance

a. Inspection Scope

The inspectors reviewed operability determinations, completed surveillances, vendor manual information, associated calculations, performance test results and cooler inspection results associated with the 2B Residual Heat Removal (RHR) heat exchanger and the DG common to both units (0 DG) heat exchanger. These heat exchangers were chosen based on their risk significance in the licensees probabilistic safety analysis, their important safety-related mitigating system support functions and their relatively low margin.

For the 2B RHR and the 0 DG heat exchangers, the inspectors verified that testing, inspection, maintenance, and monitoring of biotic fouling and macrofouling programs were adequate to ensure proper heat transfer. This was accomplished by verifying the test method used was consistent with accepted industry practices, or equivalent, the test conditions were consistent with the selected methodology, the test acceptance criteria were consistent with the design basis values, and results of heat exchanger performance testing. The inspectors also verified that the test results appropriately considered differences between testing conditions and design conditions, the frequency of testing based on trending of test results was sufficient to detect degradation prior to loss of heat removal capabilities below design basis values and test results considered test instrument inaccuracies and differences.

For the 2B RHR and the 0 DG heat exchanger, the inspectors reviewed the methods and results of heat exchanger performance inspections. The inspectors verified the methods used to inspect and clean heat exchangers were consistent with as-found conditions identified and expected degradation trends and industry standards, the licensees inspection and cleaning activities had established acceptance criteria consistent with industry standards, and the as-found results were recorded, evaluated, and appropriately dispositioned such that the as-left condition was acceptable.

The inspectors verified the performance of the ultimate heat sink (UHS) and their subcomponents, including piping, intake screens, pumps, and valves, by tests or visual inspection to ensure availability and accessibility to the in-plant cooling water systems.

The inspectors reviewed the results of the licensees inspection of the UHS weirs or excavations. The inspectors verified that identified settlement or movement indicating loss of structural integrity and/or capacity was appropriately evaluated and dispositioned by the licensee. In addition, the inspectors verified the licensee ensured sufficient reservoir capacity by trending and removing debris or sediment buildup in the UHS.

The inspectors performed a system walkdown of the service water intake structure to verify the licensees assessment on structural integrity and component functionality.

This included the verification that licensee ensured proper functioning of traveling screens and strainers, and structural integrity of component mounts. In addition, the inspectors verified that service water pump bay silt accumulation is monitored, trended, and maintained at an acceptable level by the licensee, and that water level instruments are functional and routinely monitored. The inspectors also verified the licensees ability to ensure functionality during adverse weather conditions.

In addition, the inspectors reviewed condition reports related to the heat exchangers/coolers and heat sink performance issues to verify that the licensee had an appropriate threshold for identifying issues and to evaluate the effectiveness of the corrective actions. The documents reviewed are included in the Attachment to this report.

These inspection activities constituted two heat sink inspection samples as defined in IP 71111.07-05.

b. Findings

No findings of significance were identified

1R11 Licensed Operator Requalification Program

.1 Resident Inspector Quarterly Review

a. Inspection Scope

On September 16, 2008, the inspectors observed a crew of licensed operators in the plants simulator during licensed operator requalification examinations to verify that operator performance was adequate, evaluators were identifying and documenting crew performance problems, and training was being conducted in accordance with licensee procedures. The inspectors evaluated the following areas:

  • licensed operator performance;
  • crews clarity and formality of communications;
  • ability to take timely actions in the conservative direction;
  • prioritization, interpretation, and verification of annunciator alarms;
  • correct use and implementation of abnormal and emergency procedures;
  • control board manipulations;
  • oversight and direction from supervisors; and
  • ability to identify and implement appropriate TS actions and Emergency Plan actions and notifications.

The crews performance in these areas was compared to pre-established operator action expectations and successful critical task completion requirements. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one quarterly licensed operator requalification program sample as defined in IP 71111.11.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

.1 Routine Quarterly Evaluations

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the following risk significant systems/components:

The inspectors reviewed events such as where ineffective equipment maintenance had resulted in valid or invalid automatic actuations of engineered safeguards systems and independently verified the licensees actions to address system performance or condition problems in terms of the following:

  • implementing appropriate work practices;
  • identifying and addressing common cause failures;
  • scoping of systems in accordance with the Code of Federal Regulations (CFR)10 CFR 50.65(b) of the maintenance rule;
  • characterizing system reliability issues for performance;
  • charging unavailability for performance;
  • trending key parameters for condition monitoring;
  • verifying appropriate performance criteria for structures, systems, and components (SSCs)/functions classified as (a)(2) or appropriate and adequate goals and corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability, and condition monitoring of the system. In addition, the inspectors verified maintenance effectiveness issues were entered into the CAP with the appropriate significance characterization. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two quarterly maintenance effectiveness samples as defined in IP 71111.12-05.

b. Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

.1 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensees evaluation and management of plant risk for the maintenance and emergent work activities affecting risk-significant and safety-related equipment listed below to verify that the appropriate risk assessments were performed prior to removing equipment for work:

  • Unit 1 motor-driven reactor feed pump protected pathway;
  • 2B non-essential service water jockey pump suction pipe thru-wall flaw; and
  • 1B DG protected pathway.

These activities were selected based on their potential risk significance relative to the Reactor Safety Cornerstones. As applicable for each activity, the inspectors verified that risk assessments were performed as required by 10 CFR 50.65(a)(4) and were accurate and complete. When emergent work was performed, the inspectors verified that the plant risk was promptly reassessed and managed. The inspectors reviewed the scope of maintenance work, discussed the results of the assessment with the licensees probabilistic risk analyst or shift technical advisor, and verified plant conditions were consistent with the risk assessment. The inspectors also reviewed TS requirements and walked down portions of redundant safety systems, when applicable, to verify risk analysis assumptions were valid and applicable requirements were met.

These maintenance risk assessments and emergent work control activities constituted four samples as defined in IP 71111.13-05.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

.1 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

  • Division 3 125VDC battery testing procedural adequacy;
  • Unit 1 under vessel high temperature conditions;

The inspectors selected these potential operability issues based on the risk-significance of the associated components and systems. The inspectors evaluated the technical adequacy of the evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors compared the operability and design criteria in the appropriate sections of the TS and Updated Safety Analysis Report (USAR) to the licensees evaluations, to determine whether the components or systems were operable.

Where compensatory measures were required to maintain operability, the inspectors determined whether the measures in place would function as intended and were properly controlled. The inspectors determined, where appropriate, compliance with bounding limitations associated with the evaluations. Additionally, the inspectors also reviewed a sampling of corrective action documents to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.

Documents reviewed are listed in the Attachment to this report.

This operability inspection constituted five samples as defined in IP 71111.15-05

b. Findings

No findings of significance were identified.

1R18 Plant Modifications

.1 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed the containment ventilation (VP) chiller compressor trip bypass feature modification. They compared the temporary configuration changes and associated 10 CFR 50.59 screening and evaluation information against the design basis, the UFSAR, and the TS, as applicable, to verify that the modification did not affect the operability or availability of the affected system. The inspectors also compared the licensees information to operating experience information to ensure that lessons learned from other utilities had been incorporated into the licensees decision to implement the temporary modification. Lastly, the inspectors discussed the temporary modification with operations and engineering personnel to ensure that the individuals were aware of how extended operation with the temporary modification in place could impact overall plant performance. This temporary modification was approved for installation but had not yet been installed by the licensee by the close of this inspection period.

This inspection constituted one temporary modification sample as defined in IP 71111.18-05.

b. Findings

No findings of significance were identified.

1R19 Post-Maintenance Testing (PMT)

.1 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following PMT activities to verify that procedures and test activities were adequate to ensure system operability and functional capability:

  • Drywell equipment drain sump outlet valve testing after emergent maintenance;
  • 1C LPCI motor operated valve strokes following planned electrical breaker maintenance;
  • 1B residual heat removal (RH) pump and valve run and strokes following planned electrical breaker maintenance; and
  • 0 DG emergency fast start following a planned upkeep window.

These activities were selected based upon the structure, system, or components ability to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate for the maintenance performed; acceptance criteria were clear and demonstrated operational readiness; test instrumentation was appropriate; tests were performed as written in accordance with properly reviewed and approved procedures; equipment was returned to its operational status following testing (temporary modifications or jumpers required for test performance were properly removed after test completion), and test documentation was properly evaluated. The inspectors evaluated the activities against TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC generic communications to ensure that the test results adequately ensured that the equipment met the licensing basis and design requirements. In addition, the inspectors reviewed corrective action documents associated with PMT to determine whether the licensee was identifying problems and entering them in the CAP and that the problems were being corrected commensurate with their importance to safety. Documents reviewed are listed in the Attachment to this report.

This inspection constituted five PMT samples as defined in IP 71111.19-05.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

.1 Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether risk-significant systems and equipment were capable of performing their intended safety function and to verify testing was conducted in accordance with applicable procedural and TS requirements:

  • LOS-R1-Q5; RCIC cold quick start (Routine);
  • LOS-SQ-Q1 2B SLC pump and valve quarterly (Routine);
  • LOS-VC-SR1 Control room and auxiliary electric equipment room ventilation pressurization surveillance (Routine);
  • 2B RHR quarterly American Society of Mechanical Engineers surveillance (IST);and
  • Unit 1 and Unit 2 drywell equipment drains (identified leakage) and drywell floor drains (unidentified leakage) surveillances (RCS).

The inspectors observed in plant activities and reviewed procedures and associated records to determine the following:

  • did preconditioning occur;
  • were the effects of the testing adequately addressed by control room personnel or engineers prior to the commencement of the testing;
  • were acceptance criteria clearly stated, demonstrated operational readiness, and consistent with the system design basis;
  • plant equipment calibration was correct, accurate, and properly documented;
  • as-left setpoints were within required ranges; and the calibration frequency were in accordance with TSs, the USAR, procedures, and applicable commitments;
  • measuring and test equipment calibration was current;
  • test equipment was used within the required range and accuracy; applicable prerequisites described in the test procedures were satisfied;
  • test frequencies met TS requirements to demonstrate operability and reliability; tests were performed in accordance with the test procedures and other applicable procedures; jumpers and lifted leads were controlled and restored where used;
  • test data and results were accurate, complete, within limits, and valid;
  • test equipment was removed after testing;
  • where applicable for inservice testing activities, testing was performed in accordance with the applicable version of Section XI, American Society of Mechanical Engineers code, and reference values were consistent with the system design basis;
  • where applicable, test results not meeting acceptance criteria were addressed with an adequate operability evaluation or the system or component was declared inoperable;
  • where applicable for safety-related instrument control surveillance tests, reference setting data were accurately incorporated in the test procedure;
  • where applicable, actual conditions encountering high resistance electrical contacts were such that the intended safety function could still be accomplished;
  • prior procedure changes had not provided an opportunity to identify problems encountered during the performance of the surveillance or calibration test;
  • equipment was returned to a position or status required to support the performance of its safety functions; and
  • all problems identified during the testing were appropriately documented and dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted three routine surveillance testing samples, one inservice testing sample, and one reactor coolant system leak detection inspection sample as defined in IP 71111.22, Sections -02 and -05.

b. Findings

No findings of significance were identified.

1EP6 Drill Evaluation

.1 Training Observation

a. Inspection Scope

The inspector observed a simulator training evolution for licensed operators on September 16, 2008, which required emergency plan implementation by a licensee operations crew. This evolution was planned to be evaluated and included in performance indicator (PI) data regarding drill and exercise performance. The inspectors observed event classification and notification activities performed by the crew.

The inspectors also attended the post-evolution critique for the scenario. The focus of the inspectors activities was to note any weaknesses and deficiencies in the crews performance and ensure that the licensee evaluators noted the same issues and entered them into the CAP. As part of the inspection, the inspectors reviewed the scenario package and other documents listed in the Attachment to this report.

This training inspection constituted one sample as defined in IP 71114.06-05.

b. Findings

No findings of significance were identified.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1 Plant Walkdowns and Radiation Work Permit (RWP) Reviews

a. Inspection Scope

The inspectors assessed the adequacy of the licensees internal dose assessment process for internal exposures in excess of 50 millirem committed effective dose equivalent. The inspectors also reviewed the licensees physical and programmatic controls for highly activated and/or contaminated materials (non-fuel) stored within the spent fuel pool or other storage pools.

This occupational radiation safety plant walkdown and RWP review constituted two samples as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

.2 Problem Identification and Resolution

a. Inspection Scope

The inspectors reviewed licensee documentation packages for all PI events occurring since the last inspection to determine if any of these PI events involved dose rates greater than 25 R/hr at 30 centimeters or in excess of 500 R/hr at 1 meter. Barriers were evaluated for failure and to determine if there were any barriers left to prevent personnel access. Unintended exposures exceeding 100 millirem total effective dose equivalent (or 5 Rem shallow dose equivalent or 1.5 Rem lens dose equivalent) were evaluated to determine if there were any regulatory overexposures or if there was a substantial potential for an overexposure.

This radiation safety licensee documentation inspection constituted one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

2OS2 As-Low-As-Is-Reasonably-Achievable (ALARA) Planning and Controls (71121.02)

.1 Declared Pregnant Workers

a. Inspection Scope

The inspectors reviewed dose records of declared pregnant workers for the current assessment period to verify that the exposure results and monitoring controls employed by the licensee complied with the requirements of 10 CFR Part 20. The inspectors reviewed the licensees program for declared pregnant workers. The inspectors evaluated if that program complied with the requirements of 10 CFR Part 20.

This ALARA declared pregnant workers inspection constituted one required sample as defined in IP 71121.02-5.

b. Findings

No findings of significance were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1 Unplanned Scrams per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical Hours PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the Nuclear Energy Institute (NEI) Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5 were used. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports and NRC Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted two unplanned scrams per 7000 critical hours samples as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.2 Unplanned Scrams with Complications

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams with Complications PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, event reports and NRC Integrated Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two unplanned scrams with complications samples as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.3 Unplanned Transients per 7000 Critical Hours

a. Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Transients per 7000 Critical Hours PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator narrative logs, issue reports, maintenance rule records, event reports and NRC Integrated Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two unplanned transients per 7000 critical hours samples as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.4 Reactor Coolant System (RCS) Specific Activity

a. Inspection Scope

The inspectors sampled licensee submittals for the RCS Specific Activity PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees RCS chemistry samples, TS requirements, issue reports, and event reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals.

The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator, and none were identified. In addition to record reviews, the inspectors observed a chemistry technician obtain and analyze a reactor coolant system sample. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two RCS specific activity samples as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.5 Reactor Coolant System Leakage

a. Inspection Scope

The inspectors sampled licensee submittals for the RCS Leakage PI for Unit 1 and Unit 2 for the period from the 4th quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees operator logs, RCS leakage tracking data, issue reports, event reports and NRC Integrated Inspection Reports for the period of October 2007 through June 2008 to validate the accuracy of the submittals. The inspectors also reviewed the licensees issue report database to determine if any problems had been identified with the PI data collected or transmitted for this indicator and none were identified. Documents reviewed are listed in the Attachment to this report.

This inspection constituted two RCS leakage samples as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.6 Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological Occurrences PI for the period from the 3rd quarter 2007 through the 2nd quarter 2008.

To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees assessment of the PI for occupational radiation safety to determine if indicator related data was adequately assessed and reported. To assess the adequacy of the licensees PI data collection and analyses, the inspectors discussed with radiation protection staff, the scope and breadth of its data review, and the results of those reviews. The inspectors independently reviewed electronic dosimetry dose rate and accumulated dose alarm and dose reports and the dose assignments for any intakes that occurred during the time period reviewed to determine if there were potentially unrecognized occurrences. The inspectors also conducted walkdowns of numerous locked high and very high radiation area entrances to determine the adequacy of the controls in place for these areas. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one occupational radiological occurrences sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.7 Radiological Effluent TS/Offsite Dose Calculation Manual Radiological Effluent

Occurrences

a. Inspection Scope

The inspectors sampled licensee submittals for the Radiological Effluent TS (RETS)/Offsite Dose Calculation Manual (ODCM) Radiological Effluent Occurrences PI for the period from the 3rd quarter 2007 through the 2nd quarter 2008. To determine the accuracy of the PI data reported during those periods, PI definitions and guidance contained in the NEI Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 5, were used. The inspectors reviewed the licensees issue report database and selected individual reports generated since this indicator was last reviewed to identify any potential occurrences such as unmonitored, uncontrolled, or improperly calculated effluent releases that may have impacted offsite dose. The inspectors reviewed gaseous effluent summary data and the results of associated offsite dose calculations for selected dates between from the third quarter 2007 through the second quarter 2008, to determine if indicator results were accurately reported. The inspectors also reviewed the licensees methods for quantifying gaseous and liquid effluents and determining effluent dose. Additionally, the inspectors reviewed the licensees historical 10 CFR 50.75(g) file and selectively reviewed the licensees analysis for discharge pathways resulting from a spill, leak, or unexpected liquid discharge focusing on those incidents which occurred over the last few years. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one RETS/ODCM radiological effluent occurrences sample as defined in IP 71151-05.

b. Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Physical Protection

.1 Routine Review of items Entered Into the CAP

a. Scope

As part of the various baseline inspection procedures discussed in previous sections of this report, the inspectors routinely reviewed issues during baseline inspection activities and plant status reviews to verify that they were being entered into the licensees CAP at an appropriate threshold, that adequate attention was being given to timely corrective actions, and that adverse trends were identified and addressed. Attributes reviewed included: the complete and accurate identification of the problem; that timeliness was commensurate with the safety significance; the evaluation and disposition of performance issues, generic implications, common causes, contributing factors, root causes, extent of condition reviews, and that previous occurrences reviews were proper and adequate. Also, the classification, prioritization, focus, and timeliness of corrective actions were reviewed to ensure they were commensurate with safety and sufficient to prevent recurrence of the issue. Minor issues entered into the licensees CAP as a result of the inspectors observations are included in the attached list of documents reviewed.

These routine reviews from IP 71152 for the identification and resolution of problems did not constitute any additional inspection samples. Instead, they were considered an integral part of the inspections performed during the quarter and documented in Section 1 of this report.

b. Findings

No findings of significance were identified.

.2 Daily CAP Reviews

a. Scope

In order to assist with the identification of repetitive equipment failures and specific human performance issues for follow-up, the inspectors performed a daily screening of items entered into the licensees CAP. This review was accomplished through inspection of the stations daily condition report packages.

These daily reviews were performed as defined in IP 71152 as part of the inspectors daily plant status monitoring activities and, as such, did not constitute any separate inspection samples.

b. Findings

No findings of significance were identified.

.3 Annual Review: Operator Workarounds (OWA)

a. Scope

The inspectors evaluated the licensees implementation of their process used to identify, document, track, and resolve operational challenges. Inspection activities included, but were not limited to, a review of the cumulative effects of the OWAs on system availability and the potential for improper operation of the system, for potential impacts on multiple systems, and on the ability of operators to respond to plant transients or accidents.

The inspectors performed a review of the cumulative effects of OWAs. The documents listed in the Attachment were reviewed to accomplish the objectives of the inspection procedure. The inspectors also reviewed operator challenges, which create an obstacle to normal plant operation, rather than the more severe obstacle to safe plant operation created by an OWA. The inspectors reviewed both current and historical operational challenge records to determine whether the licensee was identifying operator challenges at an appropriate threshold, had entered them into their CAP and proposed or implemented appropriate and timely corrective actions which addressed each issue.

Reviews were conducted to determine if any operator challenge could increase the possibility of an Initiating Event, if the challenge was contrary to training, required a change from long-standing operational practices, or created the potential for inappropriate compensatory actions. Additionally, all temporary modifications were reviewed to identify any potential effect on the functionality of Mitigating Systems, impaired access to equipment, or required equipment uses for which the equipment was not designed. Daily plant and equipment status logs, degraded instrument logs, and operator aids or tools being used to compensate for material deficiencies were also assessed to identify any potential sources of unidentified operator workarounds. In addition, interviews were conducted with equipment operators and licensed control room operators to determine if longstanding workarounds existed and had in turn been proceduralized into a part of accepted practice.

This operator workarounds annual inspection review constituted one sample as defined in IP 71152.

b. Findings

No findings of significance were identified.

.4 Annual Review: Safety-Related Procedure Changes

a. Scope

The inspectors reviewed a sample of approximately 100 issue reports associated with revisions to plant procedures that were associated with safety-related components or emergency operations to evaluate whether the licensees process to identify, prioritize and resolve changes needed for those procedures was adequate. Specifically, the inspectors selected procedural changes for which the due dates were moved by more than six months and revisions that would directly impact Emergency Operating Procedures. The inspectors evaluated the validity of extending the due date on a needed revision of a safety-related procedure and ensured the revisions were timely and commensurate with the safety significance of the issue. Additionally, the inspectors verified that established corrective actions by the licensee for the safety-related procedures were appropriately focused to correct the problem.

b.

Observations The inspectors noted that the licensee properly identified deficiencies in their procedures; however, the process for prioritizing and resolving the changes lacked some organization. Specifically, it was the responsibility of a few individuals from the Operations and Training departments to ensure that these procedure revisions were performed in a timely manner. The inspectors noticed that there was not a formal threshold or process to establish priorities for procedures needing modification other than personal discretion and foreseen or unforeseen events. Some examples of events that influenced the establishment of due dates were refueling outages, major equipment malfunctions and other NRC inspections.

The inspectors observed that the events that influenced the priority category and original due dates for the issue reports were also used as basis for adjusting the due dates when the actions required could not be completed in time. Additionally, the inspectors noted that in most of the issue reports with postponements, no written justification was provided for deferring the completion date. The inspectors interviewed the personnel in charge of these procedure changes to gather the information on each issue and assess whether the delays were handled in accordance with safety significance. From the sample selected, approximately 20 percent of the procedure changes required were deferred from the original due dates several times and in some cases they were pushed back by more than 6 months up to a year.

The inspectors concluded that the licensee identified necessary procedural changes commensurate with safety. However, due to the workload of personnel tasked with these changes, the prioritization and execution of these procedural revisions could improve by performing a more structured significance determination and by justifying due date rescheduling to better track the program. The inspectors did not identify any issues where the resolution timeliness of the issue report compromised the safety of plant operation.

This safety related procedural changes review constituted one inspection sample as defined in IP 71152.

c. Findings

No findings of significance were identified.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion

.1 (Closed) LER 05000374/2008001-00, High Pressure Core Spray System Declared

Inoperable Due to Failed Room Ventilation Supply Fan

a. Inspection Scope

On June 11, 2008, the supply fan for the Division 3 switchgear room ventilation system (VD) tripped unexpectedly. Division 3 switchgear supports the high pressure core spray (HPCS) system. High pressure core spray remained available to inject into the reactor vessel if needed, but was declared inoperable due to potential room heat-up with the rooms ventilation failed. As HPCS is a single train system, this failure resulted in a complete loss of system function, requiring the licensee to make an eight hour notification to the NRC under 10 CFR 50.72(b)(3)(v)(D). This event was also classified as a Safety System Functional Failure. The failure mechanism was identified by the licensee as a phase to ground short on the fans motor winding. The licensee determined the apparent cause of the motor winding failure to be a lack of a time-based refurbishment/replacement program for high duty cycle (continuously run) motors. The motor in question received periodic greasing of its bearings and quarterly vibration analysis, but no refurbishment/ replacement schedule had been established. This component was from original construction (approximately 25 years old) and vendor environmental qualification records analyzed that this component was expected to last for the licensed lifetime of the plant (40 years).

During the apparent cause investigation, the licensee identified Electric Power Research Institute (EPRI) guidance that revealed that high duty cycle motors in low power applications, such as ventilation fans, have been known to show signs of electrical degradation beginning at approximately 20 years of service. As a corrective action, the licensee established a 20 year refurbishment/replacement criteria for the supply fan in question. The licensee performed an extent of condition review of all 480 volt motors site wide extending the 20 year criterion to all critical (safety/risk significant), high duty cycle, single train, and short duration TS shutdown time clock (less than or equal to seven days) motor driven components. This expanded the motor population to four total components (the supply and return fans associated with each units Division 3 VD system). The inspectors review of the EPRI operating experience showed it to be general in nature, lacking the specificity that would reasonably cause the licensee to reevaluate previous vendor lifetime qualification data and as such the failure to establish a refurbishment/replacement criteria based on industry experience was not considered a performance deficiency. Documents reviewed in this inspection are listed in the

. This LER is closed.

This event follow-up review constituted one sample as defined in Inspection Procedure 71153-05.

b. Findings

No findings of significance were identified.

4OA5 Other

Cornerstone: Physical Protection

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities

a. Inspection Scope

During the inspection period, the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

The inspectors also reviewed a report of the results of a survey of the site security organization relative to its safety conscious work environment. The inspectors considered whether the surveys were conducted in a manner that encouraged candid and honest feedback. The results were reviewed to determine whether adequate number of staff responded to the survey. The inspectors also reviewed Exelons self-assessment of the survey results and verified that any issues or areas for improvement were entered into the CAP for resolution.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors normal plant status review and inspection activities.

b. Findings

No findings of significance were identified.

4OA6 Management Meetings

.1

Exit Meeting Summary

On October 2, 2008, the inspectors presented the inspection results to Site Vice President, Mr. Daniel Enright, and other members of the licensee staff. The licensee acknowledged the issues presented. The inspectors confirmed that none of the potential report input discussed was considered proprietary.

.2 Interim Exit Meetings

Interim exits were conducted for:

  • The results of the heat sink performance inspection with the Plant Manager, Mr. D. Rhoades, on July 25, 2008; and
  • The results of the radiation protection inspection with the Plant Manager, Mr. D. Rhodes, on August 29, 2008.

The inspectors confirmed that none of the potential report input discussed was considered proprietary.

4OA7 Licensee-Identified Violations

None.

ATTACHMENT:

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

D. Enright, Site Vice President
D. Rhoades, Plant Manager
J. Bashor, Site Engineering Director
L. Blunk, Operations Training Manager
S. Wilkinson, Chemistry Manager
H. Do, Corporate Inservice Inspection Manager
B. Ginter, Engineering Programs Manager
F. Gogliotti, System Engineering Senior Manager
W. Hilton, Engineering Supervisor - Mechanical/Structural
K. Ihnen, Nuclear Oversight Manager
A. Kochis, Inservice Inspection Engineer
R. Leasure, Radiation Protection Manager
S. Marik, Operations Director
J. Miller, NDE Level III
B. Rash, Maintenance Director
J. Rommel, Design Engineering Senior Manager
K. Rusley, Emergency Preparedness Manager
J. Shields, Inservice Inspection Program Supervisor
T. Simpkin, Regulatory Assurance Manager
H. Vinyard, Shift Operations Superintendent
G. Wilhelmsen, Design Manager
J. White, Site Training Director
C. Wilson, Station Security Manager
D. Amezaga, GL 89-13 Program Owner
J.C. Feeney, NOS Lead Assessor
D. Henly, Design Engineer

Nuclear Regulatory Commission

K. Riemer, Chief, Reactor Projects Branch 2

LIST OF ITEMS

OPENED, CLOSED AND DISCUSSED

Opened

None.

Closed

05000374/2008001-00 LER High Pressure Core Spray System Declared Inoperable Due to Failed Room Ventilation Supply Fan (4OA3)

Discussed

None.

LIST OF DOCUMENTS REVIEWED