IR 05000461/2009006: Difference between revisions
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
StriderTol (talk | contribs) (StriderTol Bot change) |
||
| (6 intermediate revisions by the same user not shown) | |||
| Line 1: | Line 1: | ||
{{Adams|number = ML090760965}} | {{Adams | ||
| number = ML090760965 | |||
| issue date = 03/17/2009 | |||
| title = IR 05000461-09-006 (Drs), on 01/26/2009 - 02/13/2009, Clinton Power Station, Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications | |||
| author name = Daley R | |||
| author affiliation = NRC/RGN-III/DRS/EB3 | |||
| addressee name = Pardee C | |||
| addressee affiliation = Exelon Generation Co, LLC, Exelon Nuclear | |||
| docket = 05000461 | |||
| license number = NPF-062 | |||
| contact person = | |||
| document report number = IR-09-006 | |||
| document type = Inspection Report, Letter | |||
| page count = 16 | |||
}} | |||
{{IR-Nav| site = 05000461 | year = 2009 | report number = 006 }} | {{IR-Nav| site = 05000461 | year = 2009 | report number = 006 }} | ||
=Text= | =Text= | ||
{{#Wiki_filter | {{#Wiki_filter:March 17, 2009 | ||
==SUBJECT:== | |||
CLINTON POWER STATION, EVALUATION OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000461/2009006(DRS) | |||
==Dear Mr. Pardee:== | |||
On February 13, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications Inspection at your Clinton Power Station. The enclosed report documents the inspection results, which were discussed on February 13, 2009, with Mr. F. A. Kearney and other members of your staff. | |||
This inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license. | |||
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no findings of significance were identified. | |||
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | |||
Sincerely,/RA/ Robert Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No. 50-461 License No. NPF-62 | Sincerely, | ||
/RA/ | |||
Robert Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No. 50-461 License No. NPF-62 | |||
===Enclosure:=== | ===Enclosure:=== | ||
Inspection Report No. 05000461/2009006(DRS) | Inspection Report No. 05000461/2009006(DRS) | ||
w/Attachment: Supplemental Information DISTRIBUTION: | |||
See next page | |||
Letter to Mr. Charles Pardee from Mr. Robert Daley dated March 17, 2009. | |||
SUBJECT: CLINTON POWER STATION, EVALUATIONS OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000461/2009006 (DRS) | SUBJECT: | ||
CLINTON POWER STATION, EVALUATIONS OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000461/2009006 (DRS) | |||
REGION III== | |||
Licensee: Exelon Generation Company, LLC Facility: Clinton Power Station Location: Clinton, IL Dates: January 26, 2009 through February 13, 2009 Inspectors: Alan Dahbur, Senior Reactor Inspector (Lead) Caroline Acosta, Senior Reactor Inspector George M. Hausman, Senior Reactor Inspector Observer: Jasmine Gilliam, Reactor Engineer Approved by: R. Daley, Chief Engineering Branch 3 Division of Reactor Safety (DRS)Enclosure | Docket No: | ||
50-461 License No: | |||
NPF-62 Report No: | |||
05000461/2009006(DRS) | |||
Licensee: | |||
Exelon Generation Company, LLC Facility: | |||
Clinton Power Station Location: | |||
Clinton, IL Dates: | |||
January 26, 2009 through February 13, 2009 Inspectors: | |||
Alan Dahbur, Senior Reactor Inspector (Lead) | |||
Caroline Acosta, Senior Reactor Inspector | |||
George M. Hausman, Senior Reactor Inspector Observer: | |||
Jasmine Gilliam, Reactor Engineer Approved by: | |||
R. Daley, Chief Engineering Branch 3 Division of Reactor Safety (DRS) | |||
Enclosure | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
IR 05000461/2009006 (DRS); 01/26/2009 - 02/13/2009; Clinton Power Station; Evaluations of | IR 05000461/2009006 (DRS); 01/26/2009 - 02/13/2009; Clinton Power Station; Evaluations of | ||
=== | Changes, Tests, or Experiments and Permanent Plant Modifications. | ||
This report covers a two-week announced baseline inspection on Evaluations of Changes, | |||
Tests, or Experiments and Permanent Plant Modifications. The inspection was conducted by Region III based engineering inspectors. Based on the results of this inspection, no findings of significance were identified. The significance of most findings is indicated by their color (Green, | |||
White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006. | |||
===NRC-Identified=== | |||
and Self-Revealed Findings | and Self-Revealed Findings | ||
===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity No findings of significance were identified. | ===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity=== | ||
No findings of significance were identified. | |||
=== | ===Licensee-Identified Violations=== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
=REPORT DETAILS= | =REPORT DETAILS= | ||
==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
===Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity=== | |||
{{a|1R17}} | |||
==1R17 Evaluation of Changes, Tests, or Experiments and Permanent Plant Modifications== | ==1R17 Evaluation of Changes, Tests, or Experiments and Permanent Plant Modifications== | ||
{{IP sample|IP=IP 71111.17}} | {{IP sample|IP=IP 71111.17}} | ||
===.1 Evaluation of Changes, Tests, or Experiments=== | ===.1 Evaluation of Changes, Tests, or Experiments=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
From January 26, 2009 through February 13, 2009, the inspectors reviewed two safety evaluations (SEs) performed pursuant to 10 CFR 50.59 to determine if the evaluations were adequate and that prior NRC approval was obtained as appropriate. The inspectors also reviewed 15 screenings and two equivalency evaluations where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to determine if: | From January 26, 2009 through February 13, 2009, the inspectors reviewed two safety evaluations (SEs) performed pursuant to 10 CFR 50.59 to determine if the evaluations were adequate and that prior NRC approval was obtained as appropriate. The inspectors also reviewed 15 screenings and two equivalency evaluations where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to determine if: | ||
| Line 59: | Line 98: | ||
* the safety issue requiring the change, tests or experiment was resolved; | * the safety issue requiring the change, tests or experiment was resolved; | ||
* the licensee conclusions for evaluations of changes, tests, or experiments were correct and consistent with 10 CFR 50.59; and | * the licensee conclusions for evaluations of changes, tests, or experiments were correct and consistent with 10 CFR 50.59; and | ||
* the design and licensing basis documentation was updated to reflect the change. The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, | * the design and licensing basis documentation was updated to reflect the change. | ||
The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations, and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, 10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments. | |||
This inspection constituted two samples of evaluations and 17 samples of changes as defined in IP 71111.17-04. | |||
====b. Findings==== | ====b. Findings==== | ||
| Line 65: | Line 108: | ||
===.2 Permanent Plant Modifications=== | ===.2 Permanent Plant Modifications=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
From January 26, 2009 through February 13, 2009, the inspectors reviewed 13 permanent plant modifications that had been installed in the plant during the last three years. This review included in-plant walkdowns for portions of the modified Emergency Diesel Generator Exhaust System and Emergency Diesel Generator Fuel Oil Day Tank System. The modifications were selected based upon risk significance, safety significance, and complexity. The inspectors reviewed the modifications selected to determine if: | From January 26, 2009 through February 13, 2009, the inspectors reviewed 13 permanent plant modifications that had been installed in the plant during the last three years. This review included in-plant walkdowns for portions of the modified Emergency Diesel Generator Exhaust System and Emergency Diesel Generator Fuel Oil Day Tank System. The modifications were selected based upon risk significance, safety significance, and complexity. The inspectors reviewed the modifications selected to determine if: | ||
| Line 72: | Line 114: | ||
* the procedures and training plans affected by the modification have been adequately updated; | * the procedures and training plans affected by the modification have been adequately updated; | ||
* the test documentation as required by the applicable test programs has been updated; and | * the test documentation as required by the applicable test programs has been updated; and | ||
* post-modification testing adequately verified system operability and/or functionality. The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an attachment to this report. This inspection constituted 13 permanent plant modification samples as defined in IP 71111.17-04. | * post-modification testing adequately verified system operability and/or functionality. | ||
The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an attachment to this report. | |||
This inspection constituted 13 permanent plant modification samples as defined in IP 71111.17-04. | |||
====b. Findings==== | ====b. Findings==== | ||
| Line 79: | Line 125: | ||
==OTHER ACTIVITIES (OA)== | ==OTHER ACTIVITIES (OA)== | ||
{{a|4OA2}} | {{a|4OA2}} | ||
==4OA2 Identification and Resolution of Problems== | ==4OA2 Identification and Resolution of Problems== | ||
===.1 Routine Review of Condition Reports=== | ===.1 Routine Review of Condition Reports=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
From January 26, 2009 through February 13, 2009, the inspectors reviewed Corrective Action Process documents that identified or were related to 10 CFR 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent pant modifications and evaluations for changes, tests, or experiments issues. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the inspectors are listed in the attachment to this report. | From January 26, 2009 through February 13, 2009, the inspectors reviewed Corrective Action Process documents that identified or were related to 10 CFR 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent pant modifications and evaluations for changes, tests, or experiments issues. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the inspectors are listed in the attachment to this report. | ||
====b. Findings==== | ====b. Findings==== | ||
No findings of significance were identified. | No findings of significance were identified. | ||
{{a|4OA6}} | {{a|4OA6}} | ||
==4OA6 Meetings== | ==4OA6 Meetings== | ||
===.1=== | |||
===.1 Exit Meeting Summary=== | ===Exit Meeting Summary=== | ||
On February 13, 2009, the inspectors presented the inspection results to Mr. F. A. Kearney, and other members of the licensee staff. The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content. | On February 13, 2009, the inspectors presented the inspection results to Mr. F. A. Kearney, and other members of the licensee staff. The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content. | ||
ATTACHMENT: | ATTACHMENT: | ||
=SUPPLEMENTAL INFORMATION= | =SUPPLEMENTAL INFORMATION= | ||
==KEY POINTS OF CONTACT== | ==KEY POINTS OF CONTACT== | ||
Licensee | Licensee | ||
: [[contact::F. A. Kearney]], Site Vice President | : [[contact::F. A. Kearney]], Site Vice President | ||
: [[contact::M. E. Kanavos]], Plant Manager | : [[contact::M. E. Kanavos]], Plant Manager | ||
| Line 115: | Line 161: | ||
: [[contact::M. Hager]], Engineering | : [[contact::M. Hager]], Engineering | ||
: [[contact::J. Wilcox]], Engineering | : [[contact::J. Wilcox]], Engineering | ||
: [[contact::N. Evans]], Engineering | : [[contact::N. Evans]], Engineering | ||
Nuclear Regulatory Commission | |||
: [[contact::C. Kemker]], Senior Resident Inspector | : [[contact::C. Kemker]], Senior Resident Inspector | ||
: [[contact::R. Daley]], Chief, Engineering Branch 3, DRS | : [[contact::R. Daley]], Chief, Engineering Branch 3, DRS | ||
==LIST OF ITEMS== | ==LIST OF ITEMS== | ||
OPENED, CLOSED AND DISCUSSED Opened, Closed, and Discussed None | ===OPENED, CLOSED AND DISCUSSED=== | ||
===Opened, Closed, and Discussed=== | |||
None | |||
==LIST OF DOCUMENTS REVIEWED== | ==LIST OF DOCUMENTS REVIEWED== | ||
}} | }} | ||
Latest revision as of 12:48, 14 January 2025
| ML090760965 | |
| Person / Time | |
|---|---|
| Site: | Clinton |
| Issue date: | 03/17/2009 |
| From: | Robert Daley Engineering Branch 3 |
| To: | Pardee C Exelon Generation Co, Exelon Nuclear |
| References | |
| IR-09-006 | |
| Download: ML090760965 (16) | |
Text
March 17, 2009
SUBJECT:
CLINTON POWER STATION, EVALUATION OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000461/2009006(DRS)
Dear Mr. Pardee:
On February 13, 2009, the U.S. Nuclear Regulatory Commission (NRC) completed an Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications Inspection at your Clinton Power Station. The enclosed report documents the inspection results, which were discussed on February 13, 2009, with Mr. F. A. Kearney and other members of your staff.
This inspection examined activities conducted under your license as they relate to safety and to compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no findings of significance were identified.
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be made available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Robert Daley, Chief Engineering Branch 3 Division of Reactor Safety Docket No. 50-461 License No. NPF-62
Enclosure:
Inspection Report No. 05000461/2009006(DRS)
w/Attachment: Supplemental Information DISTRIBUTION:
See next page
Letter to Mr. Charles Pardee from Mr. Robert Daley dated March 17, 2009.
SUBJECT:
CLINTON POWER STATION, EVALUATIONS OF CHANGES, TESTS, OR EXPERIMENTS AND PERMANENT PLANT MODIFICATIONS BASELINE INSPECTION REPORT 05000461/2009006 (DRS)
REGION III==
Docket No:
50-461 License No:
NPF-62 Report No:
Licensee:
Exelon Generation Company, LLC Facility:
Clinton Power Station Location:
Clinton, IL Dates:
January 26, 2009 through February 13, 2009 Inspectors:
Alan Dahbur, Senior Reactor Inspector (Lead)
Caroline Acosta, Senior Reactor Inspector
George M. Hausman, Senior Reactor Inspector Observer:
Jasmine Gilliam, Reactor Engineer Approved by:
R. Daley, Chief Engineering Branch 3 Division of Reactor Safety (DRS)
Enclosure
SUMMARY OF FINDINGS
IR 05000461/2009006 (DRS); 01/26/2009 - 02/13/2009; Clinton Power Station; Evaluations of
Changes, Tests, or Experiments and Permanent Plant Modifications.
This report covers a two-week announced baseline inspection on Evaluations of Changes,
Tests, or Experiments and Permanent Plant Modifications. The inspection was conducted by Region III based engineering inspectors. Based on the results of this inspection, no findings of significance were identified. The significance of most findings is indicated by their color (Green,
White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
NRC-Identified
and Self-Revealed Findings
Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity
No findings of significance were identified.
Licensee-Identified Violations
No findings of significance were identified.
REPORT DETAILS
REACTOR SAFETY
Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity
1R17 Evaluation of Changes, Tests, or Experiments and Permanent Plant Modifications
.1 Evaluation of Changes, Tests, or Experiments
a. Inspection Scope
From January 26, 2009 through February 13, 2009, the inspectors reviewed two safety evaluations (SEs) performed pursuant to 10 CFR 50.59 to determine if the evaluations were adequate and that prior NRC approval was obtained as appropriate. The inspectors also reviewed 15 screenings and two equivalency evaluations where licensee personnel had determined that a 10 CFR 50.59 evaluation was not necessary. The inspectors reviewed these documents to determine if:
- the changes, tests, or experiments performed were evaluated in accordance with 10 CFR 50.59 and that sufficient documentation existed to confirm that a license amendment was not required;
- the safety issue requiring the change, tests or experiment was resolved;
- the licensee conclusions for evaluations of changes, tests, or experiments were correct and consistent with 10 CFR 50.59; and
- the design and licensing basis documentation was updated to reflect the change.
The inspectors used, in part, Nuclear Energy Institute (NEI) 96-07, Guidelines for 10 CFR 50.59 Implementation, Revision 1, to determine acceptability of the completed evaluations, and screenings. The NEI document was endorsed by the NRC in Regulatory Guide 1.187, Guidance for Implementation of 10 CFR 50.59, Changes, Tests, and Experiments, dated November 2000. The inspectors also consulted Part 9900 of the NRC Inspection Manual, 10 CFR Guidance for 10 CFR 50.59, Changes, Tests, and Experiments.
This inspection constituted two samples of evaluations and 17 samples of changes as defined in IP 71111.17-04.
b. Findings
No findings of significance were identified.
.2 Permanent Plant Modifications
a. Inspection Scope
From January 26, 2009 through February 13, 2009, the inspectors reviewed 13 permanent plant modifications that had been installed in the plant during the last three years. This review included in-plant walkdowns for portions of the modified Emergency Diesel Generator Exhaust System and Emergency Diesel Generator Fuel Oil Day Tank System. The modifications were selected based upon risk significance, safety significance, and complexity. The inspectors reviewed the modifications selected to determine if:
- the supporting design and licensing basis documentation was updated;
- the changes were in accordance with the specified design requirements;
- the procedures and training plans affected by the modification have been adequately updated;
- the test documentation as required by the applicable test programs has been updated; and
- post-modification testing adequately verified system operability and/or functionality.
The inspectors also used applicable industry standards to evaluate acceptability of the modifications. The list of modifications and other documents reviewed by the inspectors is included as an attachment to this report.
This inspection constituted 13 permanent plant modification samples as defined in IP 71111.17-04.
b. Findings
No findings of significance were identified.
OTHER ACTIVITIES (OA)
4OA2 Identification and Resolution of Problems
.1 Routine Review of Condition Reports
a. Inspection Scope
From January 26, 2009 through February 13, 2009, the inspectors reviewed Corrective Action Process documents that identified or were related to 10 CFR 50.59 evaluations and permanent plant modifications. The inspectors reviewed these documents to evaluate the effectiveness of corrective actions related to permanent pant modifications and evaluations for changes, tests, or experiments issues. In addition, corrective action documents written on issues identified during the inspection were reviewed to verify adequate problem identification and incorporation of the problems into the corrective action system. The specific corrective action documents that were sampled and reviewed by the inspectors are listed in the attachment to this report.
b. Findings
No findings of significance were identified.
4OA6 Meetings
.1
Exit Meeting Summary
On February 13, 2009, the inspectors presented the inspection results to Mr. F. A. Kearney, and other members of the licensee staff. The licensee personnel acknowledged the inspection results presented and did not identify any proprietary content.
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee
- F. A. Kearney, Site Vice President
- M. E. Kanavos, Plant Manager
- R. D. Weber, Site Engineering Director
- J. D. Ellis, Work Management Director
- J. T. Conner, Operation Director
- C. VanDenburgh, Nuclear Oversight Manager
- D. J. Kemper, Regulatory Assurance Manager
- J. M. Stovall, Radiation Protection Manager
- J. W. Rappeport, Chemistry Manager
- C. S. Williamson, Security Manager
- R. A. Schenck, Manager Site Project Manager
- B. D. Bunte, Sr. Manager Design Engineering
- R. S. Frantz, Regulatory Assurance Representative
- M. Hager, Engineering
- J. Wilcox, Engineering
- N. Evans, Engineering
Nuclear Regulatory Commission
- C. Kemker, Senior Resident Inspector
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED
Opened, Closed, and Discussed
None