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| issue date = 04/30/2009 | | issue date = 04/30/2009 | ||
| title = Errata - IR 05000335-09-002, 05000389-09-002, 05000335-09-501, 05000389-09-501, on January 1 to March 31, 2009, St. Lucie Units 1 & 2 - NRC Integrated Inspection Report | | title = Errata - IR 05000335-09-002, 05000389-09-002, 05000335-09-501, 05000389-09-501, on January 1 to March 31, 2009, St. Lucie Units 1 & 2 - NRC Integrated Inspection Report | ||
| author name = Sykes M | | author name = Sykes M | ||
| author affiliation = NRC/RGN-II/DRP/RPB3 | | author affiliation = NRC/RGN-II/DRP/RPB3 | ||
| addressee name = Nazar M | | addressee name = Nazar M | ||
| Line 18: | Line 18: | ||
=Text= | =Text= | ||
{{#Wiki_filter: | {{#Wiki_filter:April 30, 2009 | ||
==SUBJECT:== | |||
ST. LUCIE NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000335/2009002, 05000389/2009002 | |||
SUBJECT: ST. LUCIE NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000335/2009002, 05000389/2009002 | ==Dear Mr. Nazar:== | ||
March 31, 2009 | |||
==SUBJECT:== | |||
ERRATA - ST. LUCIE NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT NOS. 05000335/2009002, 05000389/2009002 AND 5000335/2009501, 05000389/2009501 | |||
==Dear Mr. Nazar:== | ==Dear Mr. Nazar:== | ||
On March 31, 2009, the US Nuclear Regulatory Commission (NRC) completed an inspection at your St. Lucie Plant. The enclosed integrated inspection report documents the inspection findings which were discussed on April 2, 2009, with Mr. Johnston and other members of your staff. The inspection examined activities conducted under your license as they related to safety and compliance with the | On March 31, 2009, the US Nuclear Regulatory Commission (NRC) completed an inspection at your St. Lucie Plant. The enclosed integrated inspection report documents the inspection findings which were discussed on April 2, 2009, with Mr. Johnston and other members of your staff. | ||
The inspection examined activities conducted under your license as they related to safety and compliance with the Commissions rules and regulations and with the conditions of your license. | |||
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. | The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel. | ||
This report documents three NRC identified findings and one self-revealing finding, all of very low safety significance (Green). Additionally, one licensee-identified violation which was determined to be of very low safety significance is listed in Section 4OA7 of this report. These findings were determined to involve violations of NRC requirements. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating the findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV or disagree with an assigned cross- | This report documents three NRC identified findings and one self-revealing finding, all of very low safety significance (Green). Additionally, one licensee-identified violation which was determined to be of very low safety significance is listed in Section 4OA7 of this report. These findings were determined to involve violations of NRC requirements. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating the findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV or disagree with an assigned cross-cutting aspect in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial or disagreement, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the St. Lucie facility. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the St. Lucie Nuclear Plant. The information you provide will be considered in accordance with Inspection Manual Chapter 0305 | ||
cutting aspect in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial or disagreement, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the St. Lucie facility. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the St. Lucie Nuclear Plant. The information you provide will be considered in accordance with Inspection Manual Chapter 0305 | |||
FP&L | |||
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | |||
Sincerely, | |||
/RA/ | |||
Marvin D. Sykes, Chief | |||
Rector Projects Branch 3 | |||
Division of Reactor Projects | |||
Docket Nos.: 50-335, 50-389 License Nos.: DPR-67, NPF-16 | |||
===Enclosure:=== | ===Enclosure:=== | ||
Inspection Report 05000335/2009002, 05000389/2009002 | Inspection Report 05000335/2009002, 05000389/2009002 | ||
w/Attachment: Supplemental Information | |||
Supplemental Information | |||
REGION II== | |||
Docket Nos: | |||
50-335, 50-389 | |||
=== | License Nos: | ||
DPR-67, NPF-16 | |||
Report No: | |||
05000335/2009002, 05000389/2009002 | |||
Licensee: | |||
Florida Power & Light Company (FP&L) | |||
Facility: | |||
St. Lucie Nuclear Plant, Units 1 & 2 | |||
Location: | |||
6351 South Ocean Drive Jensen Beach, FL 34957 | |||
Dates: | |||
January 1 to March 31, 2009 | |||
Inspectors: | |||
T. Hoeg, Senior Resident Inspector | |||
S. Sanchez, Resident Inspector | |||
S. Ninh, Senior Project Engineer | |||
L. Miller, Senior Reactor Inspector | |||
R. Bernhard, Senior Reactor Analyst | |||
Approved by: | |||
M. Sykes, Chief Reactor Projects Branch 3 Division of Reactor Projects | |||
Enclosure U.S. NUCLEAR REGULATORY COMMISSION | |||
==REGION II== | |||
Docket Nos: | |||
50-335, 50-389 | |||
License Nos: | |||
DPR-67, NPF-16 | |||
Report No: | |||
05000335/2009002, 05000389/2009002 and | |||
05000335/2009501, 05000389/2009501 | |||
Licensee: | |||
Florida Power & Light Company (FP&L) | |||
Facility: | |||
St. Lucie Nuclear Plant, Units 1 & 2 | |||
Location: | |||
6351 South Ocean Drive Jensen Beach, FL 34957 | |||
Dates: | |||
January 1 to March 31, 2009 | |||
Inspectors: | |||
T. Hoeg, Senior Resident Inspector | |||
S. Sanchez, Resident Inspector | |||
S. Ninh, Senior Project Engineer | |||
L. Miller, Senior Reactor Inspector | |||
R. Bernhard, Senior Reactor Analyst | |||
Approved by: M. Sykes, Chief Reactor Projects Branch 3 Division of Reactor Projects | Approved by: | ||
M. Sykes, Chief Reactor Projects Branch 3 Division of Reactor Projects | |||
Enclosure SUMMARY OF FINDINGS | Enclosure SUMMARY OF FINDINGS | ||
| Line 99: | Line 152: | ||
IR 05000335/2009-002, 05000389/2009-002; 01/01/2009 - 3/31/2009; St. Lucie Nuclear Plant, Units 1 & 2; Event Follow-up, Other Activities, Surveillance Testing, Identification and Resolution of Problems. | IR 05000335/2009-002, 05000389/2009-002; 01/01/2009 - 3/31/2009; St. Lucie Nuclear Plant, Units 1 & 2; Event Follow-up, Other Activities, Surveillance Testing, Identification and Resolution of Problems. | ||
The report covered a three month period of inspection by resident inspectors and several region based inspectors. The significance of most findings is identified by their color (Green, White, Yellow, Red) using IMC 0609, | The report covered a three month period of inspection by resident inspectors and several region based inspectors. The significance of most findings is identified by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, and Revision 4, dated December 2006. | ||
A. | |||
Inspector Identified & Self-Revealing Findings | |||
Cornerstone: Initiating Events | |||
Green. A self-revealing finding was identified for failure to implement adequate process controls to minimize risk during maintenance on the Unit 2, 5B feedwater heater high level limit switch resulting in a manual reactor trip on June 4, 2008. No violations of NRC requirements were identified because the feedwater heater drain system is non-safety related. The licensee entered the issue into the corrective action program as condition report (CR) 2008-18858. Corrective actions included development of specific procedural direction for controlling and insulating energized control circuit leads during work evolutions using the risk management process, design modifications to address vulnerability when performing maintenance on level switches, and evaluation of industry best practices for training and handling of energized leads. | |||
The finding was more than minor because it resulted in a manual reactor trip. The finding was associated with the human performance attribute and affected the Initiating Events cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as at power operations. Using the NRC Manual Chapter 0609, ASignificance Determination Process,@ Attachment 609.04, Phase 1 screening worksheet, the finding was determined to be of very low safety significance because it was a transient initiator but did not increase the likelihood that mitigation equipment would not be available. The cause of the finding is related to the cross-cutting area of Human Performance, with a work control component. Specifically, the licensee did not adequately plan work activities to minimize the risk of grounding the energized leads (H.3(a)). (Section 4OA3). | The finding was more than minor because it resulted in a manual reactor trip. The finding was associated with the human performance attribute and affected the Initiating Events cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as at power operations. Using the NRC Manual Chapter 0609, ASignificance Determination Process,@ Attachment 609.04, Phase 1 screening worksheet, the finding was determined to be of very low safety significance because it was a transient initiator but did not increase the likelihood that mitigation equipment would not be available. The cause of the finding is related to the cross-cutting area of Human Performance, with a work control component. Specifically, the licensee did not adequately plan work activities to minimize the risk of grounding the energized leads (H.3(a)). (Section 4OA3). | ||
Cornerstone: Mitigating Systems Green. The inspectors identified a Green noncited violation of Technical Specifications 3.8.1, | Cornerstone: Mitigating Systems | ||
Green. The inspectors identified a Green noncited violation of Technical Specifications 3.8.1, AC Sources, for failure to perform a required monthly surveillance test in its entirety. Specifically, the inspectors identified that St. Lucie has not performed Unit 1 Emergency Diesel Generator (EDG) technical specification (TS) surveillance requirement 4.8.1.1.2 as written to verify the fuel oil transfer pumps will transfer fuel from | |||
Enclosure SUMMARY OF FINDINGS | |||
IR 05000335/2009-002, 05000389/2009-002; 01/01/2009 - 3/31/2009; and IR 05000335/2009-501, 05000389/2009-501; 02/09/2009 - 02/13/2009, St. Lucie Nuclear Plant, Units 1 & 2; Event Follow-up, Other Activities, Surveillance Testing, Identification and Resolution of Problems. | IR 05000335/2009-002, 05000389/2009-002; 01/01/2009 - 3/31/2009; and IR 05000335/2009-501, 05000389/2009-501; 02/09/2009 - 02/13/2009, St. Lucie Nuclear Plant, Units 1 & 2; Event Follow-up, Other Activities, Surveillance Testing, Identification and Resolution of Problems. | ||
The report covered a three month period of inspection by resident inspectors and several region based inspectors. The significance of most findings is identified by their color (Green, White, Yellow, Red) using IMC 0609, | The report covered a three month period of inspection by resident inspectors and several region based inspectors. The significance of most findings is identified by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, and Revision 4, dated December 2006. | ||
B. Inspector Identified & Self-Revealing Findings Cornerstone: Initiating Events Green. A self-revealing finding was identified for failure to implement adequate process controls to minimize risk during maintenance on the Unit 2, 5B feedwater heater high level limit switch resulting in a manual reactor trip on June 4, 2008. No violations of NRC requirements were identified because the feedwater heater drain system is non-safety related. The licensee entered the issue into the corrective action program as condition report (CR) 2008-18858. Corrective actions included development of specific procedural direction for controlling and insulating energized control circuit leads during work evolutions using the risk management process, design modifications to address vulnerability when performing maintenance on level switches, and evaluation of industry best practices for training and handling of energized leads. | B. | ||
Inspector Identified & Self-Revealing Findings | |||
Cornerstone: Initiating Events | |||
Green. A self-revealing finding was identified for failure to implement adequate process controls to minimize risk during maintenance on the Unit 2, 5B feedwater heater high level limit switch resulting in a manual reactor trip on June 4, 2008. No violations of NRC requirements were identified because the feedwater heater drain system is non-safety related. The licensee entered the issue into the corrective action program as condition report (CR) 2008-18858. Corrective actions included development of specific procedural direction for controlling and insulating energized control circuit leads during work evolutions using the risk management process, design modifications to address vulnerability when performing maintenance on level switches, and evaluation of industry best practices for training and handling of energized leads. | |||
The finding was more than minor because it resulted in a manual reactor trip. The finding was associated with the human performance attribute and affected the Initiating Events cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as at power operations. Using the NRC Manual Chapter 0609, ASignificance Determination Process,@ Attachment 609.04, Phase 1 screening worksheet, the finding was determined to be of very low safety significance because it was a transient initiator but did not increase the likelihood that mitigation equipment would not be available. The cause of the finding is related to the cross-cutting area of Human Performance, with a work control component. Specifically, the licensee did not adequately plan work activities to minimize the risk of grounding the energized leads (H.3(a)). (Section 4OA3). | The finding was more than minor because it resulted in a manual reactor trip. The finding was associated with the human performance attribute and affected the Initiating Events cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as at power operations. Using the NRC Manual Chapter 0609, ASignificance Determination Process,@ Attachment 609.04, Phase 1 screening worksheet, the finding was determined to be of very low safety significance because it was a transient initiator but did not increase the likelihood that mitigation equipment would not be available. The cause of the finding is related to the cross-cutting area of Human Performance, with a work control component. Specifically, the licensee did not adequately plan work activities to minimize the risk of grounding the energized leads (H.3(a)). (Section 4OA3). | ||
Cornerstone: Mitigating Systems Green. The inspectors identified a Green noncited violation of Technical Specifications 3.8.1, | Cornerstone: Mitigating Systems | ||
Green. The inspectors identified a Green noncited violation of Technical Specifications 3.8.1, AC Sources, for failure to perform a required monthly surveillance test in its entirety. Specifically, the inspectors identified that St. Lucie has not performed Unit 1 Emergency Diesel Generator (EDG) technical specification (TS) surveillance requirement 4.8.1.1.2 as written to verify the fuel oil transfer pumps will transfer fuel from | |||
}} | }} | ||
Latest revision as of 09:34, 14 January 2025
| ML092430406 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 04/30/2009 |
| From: | Marvin Sykes NRC/RGN-II/DRP/RPB3 |
| To: | Nazar M Florida Power & Light Co |
| References | |
| IR-09-002, IR-09-501 | |
| Download: ML092430406 (10) | |
Text
April 30, 2009
SUBJECT:
ST. LUCIE NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT 05000335/2009002, 05000389/2009002
Dear Mr. Nazar:
March 31, 2009
SUBJECT:
ERRATA - ST. LUCIE NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT NOS. 05000335/2009002, 05000389/2009002 AND 5000335/2009501, 05000389/2009501
Dear Mr. Nazar:
On March 31, 2009, the US Nuclear Regulatory Commission (NRC) completed an inspection at your St. Lucie Plant. The enclosed integrated inspection report documents the inspection findings which were discussed on April 2, 2009, with Mr. Johnston and other members of your staff.
The inspection examined activities conducted under your license as they related to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
This report documents three NRC identified findings and one self-revealing finding, all of very low safety significance (Green). Additionally, one licensee-identified violation which was determined to be of very low safety significance is listed in Section 4OA7 of this report. These findings were determined to involve violations of NRC requirements. However, because of the very low safety significance and because they are entered into your corrective action program, the NRC is treating the findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV or disagree with an assigned cross-cutting aspect in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial or disagreement, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the St. Lucie facility. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at the St. Lucie Nuclear Plant. The information you provide will be considered in accordance with Inspection Manual Chapter 0305
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Marvin D. Sykes, Chief
Rector Projects Branch 3
Division of Reactor Projects
Docket Nos.: 50-335, 50-389 License Nos.: DPR-67, NPF-16
Enclosure:
Inspection Report 05000335/2009002, 05000389/2009002
w/Attachment: Supplemental Information
REGION II==
Docket Nos:
50-335, 50-389
License Nos:
Report No:
05000335/2009002, 05000389/2009002
Licensee:
Florida Power & Light Company (FP&L)
Facility:
St. Lucie Nuclear Plant, Units 1 & 2
Location:
6351 South Ocean Drive Jensen Beach, FL 34957
Dates:
January 1 to March 31, 2009
Inspectors:
T. Hoeg, Senior Resident Inspector
S. Sanchez, Resident Inspector
S. Ninh, Senior Project Engineer
L. Miller, Senior Reactor Inspector
R. Bernhard, Senior Reactor Analyst
Approved by:
M. Sykes, Chief Reactor Projects Branch 3 Division of Reactor Projects
Enclosure U.S. NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos:
50-335, 50-389
License Nos:
Report No:
05000335/2009002, 05000389/2009002 and
05000335/2009501, 05000389/2009501
Licensee:
Florida Power & Light Company (FP&L)
Facility:
St. Lucie Nuclear Plant, Units 1 & 2
Location:
6351 South Ocean Drive Jensen Beach, FL 34957
Dates:
January 1 to March 31, 2009
Inspectors:
T. Hoeg, Senior Resident Inspector
S. Sanchez, Resident Inspector
S. Ninh, Senior Project Engineer
L. Miller, Senior Reactor Inspector
R. Bernhard, Senior Reactor Analyst
Approved by:
M. Sykes, Chief Reactor Projects Branch 3 Division of Reactor Projects
Enclosure SUMMARY OF FINDINGS
IR 05000335/2009-002, 05000389/2009-002; 01/01/2009 - 3/31/2009; St. Lucie Nuclear Plant, Units 1 & 2; Event Follow-up, Other Activities, Surveillance Testing, Identification and Resolution of Problems.
The report covered a three month period of inspection by resident inspectors and several region based inspectors. The significance of most findings is identified by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, and Revision 4, dated December 2006.
A.
Inspector Identified & Self-Revealing Findings
Cornerstone: Initiating Events
Green. A self-revealing finding was identified for failure to implement adequate process controls to minimize risk during maintenance on the Unit 2, 5B feedwater heater high level limit switch resulting in a manual reactor trip on June 4, 2008. No violations of NRC requirements were identified because the feedwater heater drain system is non-safety related. The licensee entered the issue into the corrective action program as condition report (CR) 2008-18858. Corrective actions included development of specific procedural direction for controlling and insulating energized control circuit leads during work evolutions using the risk management process, design modifications to address vulnerability when performing maintenance on level switches, and evaluation of industry best practices for training and handling of energized leads.
The finding was more than minor because it resulted in a manual reactor trip. The finding was associated with the human performance attribute and affected the Initiating Events cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as at power operations. Using the NRC Manual Chapter 0609, ASignificance Determination Process,@ Attachment 609.04, Phase 1 screening worksheet, the finding was determined to be of very low safety significance because it was a transient initiator but did not increase the likelihood that mitigation equipment would not be available. The cause of the finding is related to the cross-cutting area of Human Performance, with a work control component. Specifically, the licensee did not adequately plan work activities to minimize the risk of grounding the energized leads (H.3(a)). (Section 4OA3).
Cornerstone: Mitigating Systems
Green. The inspectors identified a Green noncited violation of Technical Specifications 3.8.1, AC Sources, for failure to perform a required monthly surveillance test in its entirety. Specifically, the inspectors identified that St. Lucie has not performed Unit 1 Emergency Diesel Generator (EDG) technical specification (TS) surveillance requirement 4.8.1.1.2 as written to verify the fuel oil transfer pumps will transfer fuel from
Enclosure SUMMARY OF FINDINGS
IR 05000335/2009-002, 05000389/2009-002; 01/01/2009 - 3/31/2009; and IR 05000335/2009-501, 05000389/2009-501; 02/09/2009 - 02/13/2009, St. Lucie Nuclear Plant, Units 1 & 2; Event Follow-up, Other Activities, Surveillance Testing, Identification and Resolution of Problems.
The report covered a three month period of inspection by resident inspectors and several region based inspectors. The significance of most findings is identified by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, and Revision 4, dated December 2006.
B.
Inspector Identified & Self-Revealing Findings
Cornerstone: Initiating Events
Green. A self-revealing finding was identified for failure to implement adequate process controls to minimize risk during maintenance on the Unit 2, 5B feedwater heater high level limit switch resulting in a manual reactor trip on June 4, 2008. No violations of NRC requirements were identified because the feedwater heater drain system is non-safety related. The licensee entered the issue into the corrective action program as condition report (CR) 2008-18858. Corrective actions included development of specific procedural direction for controlling and insulating energized control circuit leads during work evolutions using the risk management process, design modifications to address vulnerability when performing maintenance on level switches, and evaluation of industry best practices for training and handling of energized leads.
The finding was more than minor because it resulted in a manual reactor trip. The finding was associated with the human performance attribute and affected the Initiating Events cornerstone objective of limiting the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as at power operations. Using the NRC Manual Chapter 0609, ASignificance Determination Process,@ Attachment 609.04, Phase 1 screening worksheet, the finding was determined to be of very low safety significance because it was a transient initiator but did not increase the likelihood that mitigation equipment would not be available. The cause of the finding is related to the cross-cutting area of Human Performance, with a work control component. Specifically, the licensee did not adequately plan work activities to minimize the risk of grounding the energized leads (H.3(a)). (Section 4OA3).
Cornerstone: Mitigating Systems
Green. The inspectors identified a Green noncited violation of Technical Specifications 3.8.1, AC Sources, for failure to perform a required monthly surveillance test in its entirety. Specifically, the inspectors identified that St. Lucie has not performed Unit 1 Emergency Diesel Generator (EDG) technical specification (TS) surveillance requirement 4.8.1.1.2 as written to verify the fuel oil transfer pumps will transfer fuel from