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{{#Wiki_filter:UNITED NUCLEAR REGULATORY  
{{#Wiki_filter:UNITED STATES 
REGION 475 ALLENDALE KING OF PRUSSIA, PA  
NUCLEAR REGULATORY COMMISSION 
October 15, 2009 Mr. Paul Harden Site Vice President  
REGION
FirstEnergy  
475 ALLENDALE ROAD 
Nuclear Operating  
KING OF PRUSSIA, PA 19406-1415 
Company Beaver Valley Power Station P. O. Box 4, Route 168 Shippingport, PA 15077  
October 15, 2009  
BEAVER VALLEY POWER STATION -NRC PROBLEM IDENTIFICATION  
Mr. Paul Harden  
AND RESOLUTION  
Site Vice President  
INSPECTION  
FirstEnergy Nuclear Operating Company
REPORT 05000334/2009008  
Beaver Valley Power Station  
AND 05000412/2009008
P. O. Box 4, Route 168  
Dear Mr. Harden: On September
Shippingport, PA 15077  
3,2009, the U.S. Nuclear Regulatory
SUBJECT: 
Commission (NRC) completed
BEAVER VALLEY POWER STATION - NRC PROBLEM IDENTIFICATION  
an inspection
AND RESOLUTION INSPECTION REPORT 05000334/2009008 AND  
at your Beaver Valley Power Station Units 1 and 2. The enclosed report documents
the inspection
results, which were discussed
on September
3,2009, with Mr. Roy Brosi and other members of your staff. This inspection
was an examination
of activities
conducted
under your license as they relate to the identification
and resolution
of problems, and compliance
with the Commission's
rules and regulations
and the conditions
of your operating
license. Within these areas, the inspection
involved examination
of selected procedures
and representative
records, observations
of activities, and interviews
with personnel.
Based on the samples selected for review, the inspection
team concluded
that FirstEnergy
Nuclear Operating
Company (FENOC) was generally
effective
in identifying, evaluating
and resolving
problems.
FENOC personnel
identified
problems at a low threshold
and entered them into the Corrective
Action Program (CAP). FENOC personnel
screened issues appropriately
for operability
and reportability, and prioritized
issues commensurate
with the safety significance
of the problems.
Root and apparent cause analyses appropriately
considered
extent of condition, generic issues, and previous occurrences.
Corrective
actions addressed
the identified
causes and were typically
implemented
in a timely manner. However, the inspectors
noted several examples for improvement
in the identification
of plant issues, and examples where evaluations
lacked rigor to fully explore the corrective
actions needed to address the issue. This report documents
one NRC-identified
finding of very low safety significance (Green). The finding was determined
to involve a violation
of NRC requirements.
However, because of its very low safety significance
and because it has been entered into your CAP, the NRC is treating this finding as a non-cited
violation (NCV), in accordance
with Section VI.A.1 of the NRC's Enforcement
Policy. If you deny this NCV, you should provide a response with the basis for your denial, within 30 days of the date of this inspection
report, to the U.S. Nuclear 
P. 2 Regulatory
Commission, ATTN.: Document Control Desk, Washington
DC 20555-0001, with copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S. Nuclear Regulatory
Commission, Washington, DC 20555-0001;
and the NRC Senior Resident Inspector
at the Beaver Valley Power Station. In addition, if you disagree with the characterization
of any finding in this report, you should provide a response within 30 days of the date of this inspection
report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Senior Resident Inspector
at the Beaver Valley Power Station. The information
you provide will be considered
in accordance
with Inspection
Manual Chapter 0305. In accordance
with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available
electronically
for public inspection
in the NRC Public Document Room or from the Publicly Available
Records (PARS) component
of the NRC's document system (ADAMS). ADAMS is accessible
from the NRC Web Site at (the Public Electronic
Reading Room). Sincerely, IRA! Raymond J. Powell, Chief Technical
Support & Assessment
Branch Division of Reactor Projects Docket Nos.: 50-334, 50-412 License Nos: DPR-66, NPF-73
Inspection
Report 05000334/2009008;
05000412/2009008  
05000412/2009008  
w/Attachment:  
Dear Mr. Harden:
Supplemental  
On September 3,2009, the U.S. Nuclear Regulatory Commission (NRC) completed an
Information  
inspection at your Beaver Valley Power Station Units 1 and 2. The enclosed report documents
cc w/encls: Distribution  
the inspection results, which were discussed on September 3,2009, with Mr. Roy Brosi and
via ListServ
other members of your staff.
P. 3 copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S. Nuclear Regulatory  
This inspection was an examination of activities conducted under your license as they relate to
Commission, Washington, DC 20555-0001;  
the identification and resolution of problems, and compliance with the Commission's rules and
and the NRC Senior Resident Inspector  
regulations and the conditions of your operating license. Within these areas, the inspection
at the Beaver Valley Power Station. In addition, if you disagree with the characterization  
involved examination of selected procedures and representative records, observations of
of any finding in this report, you should provide a response within 30 days of the date of this inspection  
activities, and interviews with personnel.
report, with the basis for your disagreement, to the Regional Administrator, Region I, and the NRC Senior Resident Inspector  
Based on the samples selected for review, the inspection team concluded that FirstEnergy
at the Beaver Valley Power Station. The information  
Nuclear Operating Company (FENOC) was generally effective in identifying, evaluating and
you provide will be considered  
resolving problems. FENOC personnel identified problems at a low threshold and entered them
in accordance  
into the Corrective Action Program (CAP). FENOC personnel screened issues appropriately for
with Inspection  
operability and reportability, and prioritized issues commensurate with the safety significance of
Manual Chapter 0305. In accordance  
the problems. Root and apparent cause analyses appropriately considered extent of condition,
with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available  
generic issues, and previous occurrences. Corrective actions addressed the identified causes
electronically  
and were typically implemented in a timely manner. However, the inspectors noted several
for public inspection  
examples for improvement in the identification of plant issues, and examples where evaluations
in the NRC Public Document Room or from the Publicly Available  
lacked rigor to fully explore the corrective actions needed to address the issue.
Records (PARS) component  
This report documents one NRC-identified finding of very low safety significance (Green). The
of the NRC's document system (ADAMS). ADAMS is accessible  
finding was determined to involve a violation of NRC requirements. However, because of its
from the NRC Web Site at http://www.nrc.gov/reading-rm/adams.html(the  
very low safety significance and because it has been entered into your CAP, the NRC is
Public Electronic  
treating this finding as a non-cited violation (NCV), in accordance with Section VI.A.1 of the
Reading Room). Sincerely, IRAJ Raymond J. Powell, Chief Technical  
NRC's Enforcement Policy. If you deny this NCV, you should provide a response with the basis
Support & Assessment  
for your denial, within 30 days of the date of this inspection report, to the U.S. Nuclear
Branch Division of Reactor Projects Docket Nos.: 50-334, 50-412 License Nos: DPR-66, NPF-73  
 
Inspection  
P. Harden 
Report 05000334/2009008;  
2
05000412/2009008  
Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001, with
w/Attachment:  
copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S.
Supplemental  
Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident
Information  
Inspector at the Beaver Valley Power Station. In addition, if you disagree with the
Distribution  
characterization of any finding in this report, you should provide a response within 30 days of
w/encl: (via e-mail) S. Collins, RA (R10RAMAILRESOURCE)  
the date of this inspection report, with the basis for your disagreement, to the Regional
M. Dapas, DRA  
Administrator, Region I, and the NRC Senior Resident Inspector at the Beaver Valley Power
D. Spindler, DRP, RI D. Lew, DRP (R1  
Station. The information you provide will be considered in accordance with Inspection Manual
P. Garrett, DRP, OA J. Clifford, DRP (R1DRPMAIL  
Chapter 0305.
RESOURCE)  
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its
L. Trocine, RI OEDO R. Bellamy, RIDSNRRPMBEAVERVAllEY  
enclosure, and your response (if any) will be available electronically for public inspection in the
RESOURCE G. Barber, ROPreportsResource@nrc.qov  
NRC Public Document Room or from the Publicly Available Records (PARS) component of the
C. Newport, Region I Docket Room (with concurrences)  
NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at
J. Greives, DRP D. Werkheiser, DRP, SRI SUNSI Review Complete:  
~=:'::'~~~~=-'-=:::'!J..!.~~=~~",-= (the Public Electronic Reading Room).
tcs (Reviewer's  
Sincerely,
IRA!
Raymond J. Powell, Chief
Technical Support & Assessment Branch
Division of Reactor Projects
Docket Nos.: 50-334, 50-412
License Nos: DPR-66, NPF-73
Enclosures: 
Inspection Report 05000334/2009008; 05000412/2009008
w/Attachment: Supplemental Information  
cc w/encls: Distribution via ListServ  
 
P. Harden 
3  
copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S.  
Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident  
Inspector at the Beaver Valley Power Station. In addition, if you disagree with the  
characterization of any finding in this report, you should provide a response within 30 days of  
the date of this inspection report, with the basis for your disagreement, to the Regional  
Administrator, Region I, and the NRC Senior Resident Inspector at the Beaver Valley Power  
Station. The information you provide will be considered in accordance with Inspection Manual
Chapter 0305.  
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its  
enclosure, and your response (if any) will be available electronically for public inspection in the  
NRC Public Document Room or from the Publicly Available Records (PARS) component of the  
NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at  
http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).  
Sincerely,  
IRAJ  
Raymond J. Powell, Chief  
Technical Support & Assessment Branch
Division of Reactor Projects  
Docket Nos.: 50-334, 50-412  
License Nos: DPR-66, NPF-73  
Enclosures: 
Inspection Report 05000334/2009008; 05000412/2009008  
w/Attachment: Supplemental Information  
Distribution w/encl: (via e-mail)  
S. Collins, RA (R10RAMAILRESOURCE)  
M. Dapas, DRA (R10RAMAILRESOURCE) 
D. Spindler, DRP, RI  
D. Lew, DRP (R1 DRPMAILRESOURCE) 
P. Garrett, DRP, OA  
J. Clifford, DRP (R1DRPMAIL RESOURCE)  
L. Trocine, RI OEDO  
R. Bellamy, DRP 
RIDSNRRPMBEAVERVAllEY RESOURCE
G. Barber, DRP 
ROPreportsResource@nrc.qov  
C. Newport, DRP 
Region I Docket Room (with concurrences)  
J. Greives, DRP  
D. Werkheiser, DRP, SRI  
SUNSI Review Complete: tcs
(Reviewer's Initials) 
ML092920008  
ML092920008  
DOCUMENT NAME: G:\DRP\BRANCH  
DOCUMENT NAME: G:\\DRP\\BRANCH TSAB\\lnspection Reports\\Beaver Valley PI&R 2009\\BV PIR 
TSAB\lnspection  
IR2009008revO.doc 
Reports\Beaver  
After declaring this document "An Official Agency Record" it will be released to the Public. 
Valley PI&R 2009\BV  
To receive acopy of this document, indicate In the box: 'C' =Copy without attachment/enclosure 'E" =Copy with attachment/enclosure "N" =No copy 
After declaring  
OFFICE:  
this document "An Official Agency Record" it will be released to the To receive a copy of this document, indicate In the box: 'C' =Copy without attachment/enclosure  
RI/DRP  
'E" =Copy with attachment/enclosure "N" =No OFFICE: RI/DRP NAME: TSetzer/tcs  
RI/DRP 
RBeliamy/rjp  
NAME:  
for DATE: 10/13109 10/14/09   
TSetzer/tcs  
Docket License Report Team  
RBeliamy/rjp for
Approved 1 U.S. NUCLEAR REGULATORY  
DATE:  
REGION 50-334, DPR-66, 05000334/2009008  
10/13109  
and  
10/14/09  
FirstEnergy  
 
Nuclear Operating  
Docket Nos.  
Company Beaver Valley Power Station, Units 1 and Post Office Box Shippingport, PA August 17 through September  
License Nos. 
3, Thomas Setzer, PE, Senior Project  
Report Nos. 
Division of Reactor Projects (DRP) Jeffery Bream, Project Engineer, DRP Elizabeth  
Licensee: 
Keighley, Reactor Inspector, DRP David Spindler, Beaver Valley Resident Inspector, DRP Raymond J. Powell, Chief Technical  
Facility: 
Support &Assessment  
Location: 
Branch Division of Reactor Projects Enclosure
Dates: 
2 SUMMARY OF FINDINGS IR 05000334/2009008, IR 05000412/2009008;  
Team Leader: 
08/17/2009  
Inspectors: 
-09/03/2009;  
Approved by: 
Beaver Valley Power Station, Units  
1  
1 & 2; Biennial Baseline Inspection  
U.S. NUCLEAR REGULATORY COMMISSION 
of the Identification  
REGION
and Resolution  
50-334, 50-412 
of Problems.  
DPR-66, NPF-73 
One finding was identified  
05000334/2009008 and 05000412/2009008 
in the area of prioritization  
FirstEnergy Nuclear Operating Company (FENOC) 
and evaluation  
Beaver Valley Power Station, Units 1 and
of issues. This team inspection  
Post Office Box
was performed  
Shippingport, PA 15077 
by three NRC regional inspectors  
August 17 through September 3, 2009 
and one resident inspector.  
Thomas Setzer, PE, Senior Project Engineer 
One finding of very low safety significance (Green) was identified  
Division of Reactor Projects (DRP)  
during this inspection  
Jeffery Bream, Project Engineer, DRP  
and was classified  
Elizabeth Keighley, Reactor Inspector, DRP  
as a non-cited  
David Spindler, Beaver Valley Resident Inspector, DRP  
violation (NCV). The significance  
Raymond J. Powell, Chief  
of most findings is indicated  
Technical Support &Assessment Branch
by their color (Green, White, Yellow, Red) using NRC Inspection  
Division of Reactor Projects  
Manual Chapter (IMC) 0609, "Significance  
Enclosure  
Determination  
 
Process" (SOP). The cross-cutting  
2  
aspect was determined  
SUMMARY OF FINDINGS  
using IMC 0305, "Operating  
IR 05000334/2009008, IR 05000412/2009008; 08/17/2009 - 09/03/2009; Beaver Valley Power  
Reactor Assessment  
Station, Units 1 & 2; Biennial Baseline Inspection of the Identification and Resolution of Problems.  
Program." Findings for which the SOP does not apply may be Green or be assigned a severity level after NRC management  
One finding was identified in the area of prioritization and evaluation of issues.  
review. The NRC's program for overseeing  
This team inspection was performed by three NRC regional inspectors and one resident  
the safe operation  
inspector. One finding of very low safety significance (Green) was identified during this  
of commercial  
inspection and was classified as a non-cited violation (NCV). The significance of most findings is  
nuclear power reactors is described  
indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter (IMC)  
in NUREG-1649, "Reactor Oversight  
0609, "Significance Determination Process" (SOP). The cross-cutting aspect was determined  
Process," Revision 4, December 2006. Identification  
using IMC 0305, "Operating Reactor Assessment Program." Findings for which the SOP does  
and Resolution  
not apply may be Green or be assigned a severity level after NRC management review. The  
of Problems The inspectors  
NRC's program for overseeing the safe operation of commercial nuclear power reactors is  
concluded  
described in NUREG-1649, "Reactor Oversight Process," Revision 4, December 2006.  
that FENOC was, in general, effective  
Identification and Resolution of Problems  
in identifying, evaluating, and resolving  
The inspectors concluded that FENOC was, in general, effective in identifying, evaluating, and  
problems.  
resolving problems. Beaver Valley personnel identified problems at a low threshold and entered  
Beaver Valley personnel  
them into the Corrective Action Program (CAP). The inspectors determined that Beaver Valley  
identified  
personnel screened issues appropriately for operability and reportability, and prioritized issues
problems at a low threshold  
commensurate with the safety significance of the problems. Root and apparent cause analyses  
and entered them into the Corrective  
appropriately considered extent of condition, generic issues, and previous occurrences. The
Action Program (CAP). The inspectors  
inspectors determined that corrective actions addressed the identified causes and were typically  
determined  
implemented in a timely manner. However, the inspectors noted one NCV of very low safety  
that Beaver Valley personnel  
significance in the area of prioritization and evaluation of issues. This issue was entered into  
screened issues appropriately  
FENOC's CAP during the inspection.  
for operability  
FENOC's audits and self-assessments reviewed by the inspectors were thorough and probing.  
and reportability, and prioritized  
Additionally, the inspectors concluded that FENOC adequately identified, reviewed, and applied  
issues commensurate  
relevant industry operating experience (OE) to the Beaver Valley Power Station. Based on  
with the safety significance  
interviews, observations of plant activities, and reviews of the CAP and the Employees Concerns
of the problems.  
Program (ECP), the inspectors did not identify any concerns with site personnel willingness to
Root and apparent cause analyses appropriately  
raise safety issues, nor did the inspectors identify conditions that could have had a negative  
considered  
impact on the site's safety conscious work environment (SCWE).  
extent of condition, generic issues, and previous occurrences.  
Cornerstone: Mitigating Systems
The inspectors  
Green. The inspectors identified an NCV of very low safety significance (Green) of  
determined  
10 CFR 50.65(a)(2), "Requirements for Monitoring the Effectiveness of Maintenance at
that corrective  
Nuclear Power Plants," due to FENOC personnel's failure to demonstrate that the  
actions addressed  
10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches was  
the identified  
effectively controlled through the performance of appropriate preventive maintenance.  
causes and were typically  
Specifically, as evidenced by repeat dual position indications of containment isolation  
implemented  
valves in the control room between 2007 and 2009 resulting in 21 unplanned entries into  
in a timely manner. However, the inspectors  
Technical Specification 3.6.3, the containment isolation valve system 10 CFR 50.65(a)(2)  
noted one NCV of very low safety significance  
performance demonstration was no longer justified in accordance with Maintenance Rule
in the area of prioritization  
Enclosure  
and evaluation  
 
of issues. This issue was entered into FENOC's CAP during the inspection.  
3  
FENOC's audits and self-assessments  
implementing procedure guidance. This should have resulted in placement of the  
reviewed by the inspectors  
containment isolation valve system in 10 CFR 50.65(a)(1) for goal setting and monitoring.  
were thorough and probing. Additionally, the inspectors  
concluded  
that FENOC adequately  
identified, reviewed, and applied relevant industry operating  
experience (OE) to the Beaver Valley Power Station. Based on interviews, observations  
of plant activities, and reviews of the CAP and the Employees  
Concerns Program (ECP), the inspectors  
did not identify any concerns with site personnel  
willingness  
to raise safety issues, nor did the inspectors  
identify conditions  
that could have had a negative impact on the site's safety conscious  
work environment (SCWE). Cornerstone:  
Mitigating  
Systems Green. The inspectors  
identified  
an NCV of very low safety significance (Green) of 10 CFR 50.65(a)(2), "Requirements  
for Monitoring  
the Effectiveness  
of Maintenance  
at Nuclear Power Plants," due to FENOC personnel's  
failure to demonstrate  
that the 10 CFR 50.65(a)(2)  
performance  
of the containment  
isolation  
valve limit switches was effectively  
controlled  
through the performance  
of appropriate  
preventive  
maintenance.  
Specifically, as evidenced by  
repeat dual position indications  
of containment  
isolation  
valves in the control room between 2007 and 2009 resulting  
in 21 unplanned  
entries into Technical  
Specification  
3.6.3, the containment  
isolation  
valve system 10 CFR 50.65(a)(2)  
performance  
demonstration  
was no longer justified  
in accordance  
with Maintenance  
Rule Enclosure   
implementing  
procedure  
guidance.  
This should have resulted in placement  
of the containment  
isolation  
valve system in 10 CFR 50.65(a)(1)  
for goal setting and monitoring.  
FENOC entered this issue into the CAP (CR 09-64040).  
FENOC entered this issue into the CAP (CR 09-64040).  
The inspectors  
The inspectors determined the finding was more than minor because it is associated with
determined  
the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely  
the finding was more than minor because it is associated  
affected the cornerstone objective of ensuring the reliability of systems that respond to  
with the Equipment  
initiating events to prevent undesirable consequences. The finding was determined to be  
Performance  
of very low safety significance (Green) because the finding did not involve a design or  
attribute  
qualification deficiency resulting in loss of operability or functionality, did not result in a  
of the Mitigating  
loss of system safety function, and did not screen as potentially risk significant due to  
Systems cornerstone  
external initiating events. The inspectors determined that this finding had a cross-cutting  
and adversely  
aspect in the "Corrective Action Program" component of the Problem Identification and
affected the cornerstone  
Resolution cross-cutting area because FENOC did not take appropriate corrective actions
objective  
to address safety issues and adverse trends associated with faulty containment isolation  
of ensuring the reliability  
valve limit switches in a timely manner, commensurate with their safety significance and
of systems that respond to initiating  
complexity [P.1(d)]. (Section 40A2.1c)  
events to prevent undesirable  
Enclosure  
consequences.  
 
The finding was determined  
.1  
to be of very low safety significance (Green) because the finding did not involve a design or qualification  
deficiency  
REPORT DETAILS  
resulting  
4.  
in loss of operability  
OTHER ACTIVITIES (OA)  
or functionality, did not result in a loss of system safety function, and did not screen as potentially  
40A2 Problem Identification and Resolution (PI&R) (71152B)  
risk significant  
Assessment of the Corrective Action Program Effectiveness  
due to external initiating  
a.  
events. The inspectors  
Inspection Scope
determined  
The inspectors reviewed FENOC's procedures that describe the CAP at the Beaver Valley  
that this finding had a cross-cutting  
Power Station. FENOC personnel identified problems by initiating condition reports (CRs)  
aspect in the "Corrective  
for conditions adverse to quality, plant equipment deficiencies, industrial or radiological  
Action Program" component  
safety concerns, and other significant issues. Condition reports were subsequently  
of the Problem Identification  
screened for operability and reportability, and categorized by significance, which included  
and Resolution  
levels SR (significant condition adverse to quality, root cause), AR (adverse condition, root  
cross-cutting  
cause), AA (adverse condition, full apparent cause), AL (adverse condition, limited  
area because FENOC did not take appropriate  
apparent cause), AF (adverse condition, fix), and AC (adverse condition, close). CRs  
corrective  
were assigned to personnel for evaluation and resolution or trending.  
actions to address safety issues and adverse trends associated  
The inspectors evaluated the process for assigning and tracking issues to ensure that  
with faulty containment  
issues were screened for operability and reportability, prioritized for evaluation and
isolation  
resolution in a timely manner commensurate with their safety significance, and tracked to  
valve limit switches in a timely manner, commensurate  
identify adverse trends and repetitive issues. In addition, the inspectors interviewed plant
with their safety significance  
staff and management to determine their understanding of, and involvement with, the  
and complexity  
CAP.  
[P.1(d)]. (Section 40A2.1c) Enclosure
The inspectors reviewed CRs selected across the seven cornerstones of safety in the  
.1 REPORT DETAILS 4. OTHER ACTIVITIES (OA) 40A2 Problem Identification  
NRC's Reactor Oversight Process (ROP) to determine if site personnel properly identified,  
and Resolution (PI&R) (71152B) Assessment  
characterized, and entered problems into the CAP for evaluation and resolution. The
of the Corrective  
inspectors selected items from functional areas that included physical security,  
Action Program Effectiveness  
emergency preparedness, engineering, maintenance, operations, and radiation safety to  
a. Inspection  
ensure that FENOC appropriately addressed problems identified in these functional areas.  
Scope The inspectors  
The inspectors selected a risk-informed sample of CRs that had been issued since the  
reviewed FENOC's procedures  
last NRC Problem Identification and Resolution (PI&R) inspection conducted in April 2007.  
that describe the CAP at the Beaver Valley Power Station. FENOC personnel  
Insights from the station's risk analyses were considered to focus the sample selection  
identified  
and plant walkdowns on risk-significant systems and components. The corrective action
problems by initiating  
review was expanded to five years for evaluation of identified concerns within CRs relative  
condition  
to radiation monitors.  
reports (CRs) for conditions  
The inspectors selected items from various processes at Beaver Valley to verify that they  
adverse to quality, plant equipment  
were appropriately considered for entry into the CAP. Specifically, the inspectors  
deficiencies, industrial  
reviewed a sample of Maintenance Rule functional failure evaluations, operability  
or radiological  
determinations, system health reports, work orders (WOs), and issues entered into the  
safety concerns, and other significant  
Employee Concerns Program (ECP). The inspectors inspected plant areas including the
issues. Condition  
turbine buildings, safeguards buildings, intake structure, emergency diesel generator  
reports were subsequently  
buildings, yard areas, security areas, and control room.  
screened for operability  
Enclosure  
and reportability, and categorized  
 
by significance, which included levels SR (significant  
5  
condition  
The inspectors reviewed CRs to assess whether FENOC personnel adequately evaluated  
adverse to quality, root cause), AR (adverse condition, root cause), AA (adverse condition, full apparent cause), AL (adverse condition, limited apparent cause), AF (adverse condition, fix), and AC (adverse condition, close). CRs were assigned to personnel  
and prioritized issues. The CRs reviewed encompassed the full range of evaluations,  
for evaluation  
including root cause analyses, full apparent cause evaluations, limited apparent cause  
and resolution  
analyses, and common cause analyses. A sample of CRs that were assigned lower  
or trending.  
levels of significance which did not include formal cause evaluations (AF and AC  
The inspectors  
significance levels) were also reviewed by the inspectors to ensure they were  
evaluated  
appropriately classified. The inspectors' review included the appropriateness of the  
the process for assigning  
assigned significance, the scope and depth of the analysis, and the timeliness of
and tracking issues to ensure that issues were screened for operability  
resolution. The inspectors assessed whether the evaluations identified likely causes for  
and reportability, prioritized  
the issues and identified appropriate corrective actions to address the identified causes.  
for evaluation  
As part of this review, the inspectors interviewed various station personnel to fully  
and resolution  
understand details within the evaluations and the proposed and completed corrective  
in a timely manner commensurate  
actions. The inspectors observed management review board (MRB) meetings in which  
with their safety significance, and tracked to identify adverse trends and repetitive  
FENOC personnel reviewed new CRs for prioritization and assignment. Further, the  
issues. In addition, the inspectors  
inspectors reviewed equipment operability determinations and extent-of-condition reviews
interviewed  
for selected CRs to verify these specific reviews adequately addressed equipment  
plant staff and management  
operability and the extent of problems.  
to determine  
The inspectors' review of CRs also focused on the associated corrective actions in order  
their understanding  
to determine whether the actions addressed the identified causes of the problems. The
of, and involvement  
inspectors reviewed CRs for adverse trends and repetitive problems to determine whether
with, the CAP. The inspectors  
corrective actions were effective in addressing the broader issues. The inspectors  
reviewed CRs selected across the seven cornerstones  
reviewed FENOC's timeliness in implementing. corrective actions and effectiveness in
of safety in the NRC's Reactor Oversight  
precluding recurrence for significant conditions adverse to quality. Lastly, the inspectors  
Process (ROP) to determine  
reviewed CRs associated with NRC non-cited violations (NCV) and findings since the last  
if site personnel  
PI&R inspection to determine whether FENOC personnel properly evaluated and resolved  
properly identified, characterized, and entered problems into the CAP for evaluation  
the issues. Specific documents reviewed during the inspection are listed in the  
and resolution.  
Attachment to this report.  
The inspectors  
b.  
selected items from functional  
Assessment  
areas that included physical security, emergency  
Effectiveness of Problem Identification  
preparedness, engineering, maintenance, operations, and radiation  
Based on the selected samples reviewed, plant walkdowns, and interviews of site  
safety to ensure that FENOC appropriately  
personnel, the inspectors determined that, in general, FENOC personnel identified  
addressed  
problems and entered them into the CAP at a low threshold. For the issues reviewed, the  
problems identified  
inspectors noted that problems or concerns had been appropriately documented in
in these functional  
enough detail to understand the issues. Approximately 19,000 CRs had been written by  
areas. The inspectors  
FENOC personnel since January 2007. The inspectors noted that the Security  
selected a risk-informed  
department had generated significantly less CRs when compared to the rest of the site.  
sample of CRs that had been issued since the last NRC Problem Identification  
Interviews with Security personnel revealed that they had received adequate training,  
and Resolution (PI&R) inspection  
displayed a willingness to raise issues, and had ample access to computers; however,  
conducted  
there was a reliance on the shift Captain to enter issues into the CAP.  
in April 2007. Insights from the station's  
The inspectors observed managers and supervisors at MRB meetings appropriately  
risk analyses were considered  
questioning and challenging CRs to ensure clarity of the issues. The inspectors  
to focus the sample selection  
determined that FENOC personnel trended equipment and programmatic issues, and CR  
and plant walkdowns  
descriptions appropriately included reference to repeat occurrences of issues. The  
on risk-significant  
Enclosure  
systems and components.  
 
The corrective  
6  
action review was expanded to five years for evaluation  
inspectors concluded that personnel were identifying trends at low levels.  
of identified  
The inspectors toured plant areas including the turbine buildings, safeguards buildings,  
concerns within CRs relative to radiation  
intake structure, emergency diesel generator buildings, yard areas, security areas and  
monitors.  
control room to determine if FENOC personnel identified plant issues at the proper  
The inspectors  
threshold. Housekeeping in all areas, with the exception of the Unit 2 intake structure,  
selected items from various processes  
was noted to be improved since the 2007 NRC PI&R inspection. During the plant  
at Beaver Valley to verify that they were appropriately  
walkdown, the inspectors identified three examples of adverse conditions that had not  
considered  
been identified by FENOC. The following issues were entered into the CAP for evaluation  
for entry into the CAP. Specifically, the inspectors  
and resolution:  
reviewed a sample of Maintenance  
Rule functional  
During an inspection of the east end of the main intake structure, the inspectors  
failure evaluations, operability  
identified an oxygen bottle strapped to an Appendix R ladder (a ladder used by  
determinations, system health reports, work orders (WOs), and issues entered into the Employee Concerns Program (ECP). The inspectors  
plant personnel for implementing the site fire protection program). Restraining the
inspected  
oxygen bottle and Appendix R ladder together in this fashion represented a minor  
plant areas including  
procedure violation of Beaver Valley procedure, 1/2-PIP-G01, "Securing  
the turbine buildings, safeguards  
Transient/Temporary/Stored Equipment in Safety-Related Areas." This issue is  
buildings, intake structure, emergency  
minor because there was no adverse impact to plant safety equipment, and there  
diesel generator  
was only minimal impact on operator fire response times. FENOC entered this  
buildings, yard areas, security areas, and control room. Enclosure   
into the CAP (CR 09-63536).  
The inspectors  
reviewed CRs to assess whether FENOC personnel  
During an inspection of the 'D' intake structure cubicle, the inspectors identified  
adequately  
rigging scaffolding with a chainfall that had been left draped over a safety related  
evaluated  
component. Scaffold contacting plant equipment represented a minor procedure  
and prioritized  
violation of Beaver Valley procedure, 1/2-ADM-0810, "Scaffold Erection and  
issues. The CRs reviewed encompassed  
Tagging." The component was not damaged nor had any reduced capability as a  
the full range of evaluations, including  
result of the contact with the chainfall. This issue is minor because there was no  
root cause analyses, full apparent cause evaluations, limited apparent cause analyses, and common cause analyses.  
loss of operability or adverse impact to the safety related component. FENOC
A sample of CRs that were assigned lower levels of significance  
entered this into the CAP (CR 09-63532).  
which did not include formal cause evaluations (AF and AC significance  
levels) were also reviewed by the inspectors  
During an inspection of the Unit 2 Safeguards Building, the inspectors identified  
to ensure they were appropriately  
four plastic buckets filled with lubricating oil totaling 20 gallons. The unattended oil
classified.  
in a safety related fire area represented a minor procedure violation of Beaver  
The inspectors'  
Valley procedure, 1/2-ADM-1906, "Control of Transient Combustible and
review included the appropriateness  
Flammable Materials." This issue is minor because the increase in combustible  
of the assigned significance, the scope and depth of the analysis, and the timeliness  
loading in the room as a result of the unattended oil did not violate the plant fire  
of resolution.  
hazard analysis. FENOC entered this into the CAP (CR 09-63441).  
The inspectors  
In accordance with NRC Inspection Manual Chapter 0612, "Power Reactor Inspection  
assessed whether the evaluations  
Reports," the above issues constitute violations of minor significance that are not subject  
identified  
to enforcement action in accordance with the NRC's Enforcement Policy.  
likely causes for the issues and identified  
Effectiveness of Prioritization and Evaluation of Issues  
appropriate  
The inspectors determined that, in general, FENOC personnel appropriately prioritized  
corrective  
and evaluated issues commensurate with their safety significance. CRs were screened  
actions to address the identified  
for operability and reportability, categorized by significance, and assigned to a department  
causes. As part of this review, the inspectors  
for evaluation and resolution. The CR screening process considered human performance  
interviewed  
issues, radiological safety concerns, repetitiveness and adverse trends. The inspectors  
various station personnel  
observed managers and supervisors at MRB meetings appropriately questioning and
to fully understand  
challenging CRs to ensure appropriate prioritization.  
details within the evaluations  
Enclosure  
and the proposed and completed  
 
corrective  
7  
actions. The inspectors  
CRs were categorized for evaluation and resolution commensurate with the significance of
observed management  
the issues. Based on the sample of CRs reviewed, the guidance provided by the FENOC  
review board (MRB) meetings in which FENOC personnel  
implementing procedures appeared sufficient to ensure consistency in categorization of
reviewed new CRs for prioritization  
the issues. Operability and reportability determinations were performed when conditions  
and assignment.  
warranted and the evaluations supported the conclusions. Causal analyses appropriately  
Further, the inspectors  
considered extent of condition, generic issues, and previous occurrences. During this  
reviewed equipment  
inspection, the inspectors noted that, in general, FENOC's root cause analyses were  
operability  
thorough, and corrective and preventive actions addressed the identified causes.  
determinations  
Additionally, the identified causes were well supported. An NCV was identified for
and extent-of-condition  
FENOC's failure to demonstrate that the 10 CFR 50.65(a)(2) performance of the  
reviews for selected CRs to verify these specific reviews adequately  
containment isolation valve limit switches was effectively controlled through the  
addressed  
performance of appropriate preventive maintenance. This NCV is discussed in the  
equipment  
findings section of this assessment area. The inspectors identified the following two
operability  
examples of issues that were not fully evaluated or prioritized for corrective action:  
and the extent of problems.  
A root cause evaluation (CR 08-39835) associated with a 2.5 inch drain down of  
The inspectors'  
the Unit 2 reactor coolant system during refueling outage 2R13 did not identify all  
review of CRs also focused on the associated  
corrective actions necessary to address all failed barriers. The inspectors noted
corrective  
that the root cause evaluation had not included corrective actions to address the  
actions in order to determine  
communication failure within operations shifts, and the work management  
whether the actions addressed  
scheduling issues which contributed to a component tagoutlctearance being
the identified  
inappropriately implemented. The issue is minor because while corrective actions
causes of the problems.  
were not assigned to address all failed barriers, FENOC had discussed  
The inspectors  
communication expectations with each operating crew and there have not been  
reviewed CRs for adverse trends and repetitive  
any repeat issues. FENOC entered these issues into the CAP (CR 09-63454 and  
problems to determine  
09-63479).  
whether corrective  
actions were effective  
The inspectors identified three CRs describing component mispositioning events
in addressing  
(CR 09-59541, CR 09-58355, and CR 09-57224) that were prioritized as CR level  
the broader issues. The inspectors  
OlAF." The failure to prioritize these CRs as a limited apparent cause (CR level  
reviewed FENOC's timeliness  
"AL") represented a minor procedure violation of Beaver Valley procedure, NOBP
in implementing.  
OP-0004, "Component Mispositioning." The inspectors reviewed NRC Inspection  
corrective  
Manual Chapter 0612, Appendix E, "Minor Examples," and determined this issue  
actions and effectiveness  
was minor because there was no loss of operability or safety impact. FENOC  
in precluding  
entered this issue into the CAP (CR 09-64004 and CR 09-63975).  
recurrence  
In accordance with NRC Inspection Manual Chapter 0612, "Power Reactor Inspection  
for significant  
Reports," these issues constitute violations of minor significance that are not subject  
conditions  
to enforcement action in accordance with the NRC's Enforcement Policy.  
adverse to quality. Lastly, the inspectors  
Effectiveness of Corrective Actions
reviewed CRs associated  
The inspectors concluded that corrective actions for identified deficiencies were generally  
with NRC non-cited  
timely and adequately implemented. For significant conditions adverse to quality,  
violations (NCV) and findings since the last PI&R inspection  
corrective actions were identified to prevent recurrence. The inspectors concluded that
to determine  
corrective actions to address NCVs and findings since the last PI&R inspection were
whether FENOC personnel  
timely and effective. The inspectors identified the following example where corrective  
properly evaluated  
actions were not fully effective in addressing an issue:  
and resolved the issues. Specific documents  
Enclosure  
reviewed during the inspection  
 
are listed in the Attachment  
8  
to this report. b. Assessment  
The inspectors reviewed corrective actions taken in response to an NCV  
Effectiveness  
documented in NRC report 05000334/05000412 2007004. CR 07-24074 was  
of Problem Identification  
written to ensure bearing temperatures would be monitored when performing  
Based on the selected samples reviewed, plant walkdowns, and interviews  
surveillance testing on the turbine driven auxiliary feedpumps (TDAFWP). The
of site personnel, the inspectors  
inspectors found that the comprehensive surveillance tests for Unit 1 and Unit 2  
determined  
(Beaver Valley procedures 10ST-24.9 and 20ST-24.4A, respectively) did not have  
that, in general, FENOC personnel  
a precaution stating that this surveillance was not suitable to be used for post  
identified  
maintenance testing as there is no guidance prescribed to monitor and achieve  
problems and entered them into the CAP at a low threshold.  
steady bearing temperatures. The inspectors determined that the issue was minor  
For the issues reviewed, the inspectors  
because the preventive maintenance work order had contained the appropriate  
noted that problems or concerns had been appropriately  
guidance. FENOC entered this issue into the CAP (CR 09-64015).  
documented  
c.  
in enough detail to understand  
Findings  
the issues. Approximately  
Introduction: The inspectors identified an NCV of very low safety significance (Green) of  
19,000 CRs had been written by FENOC personnel  
10 CFR 50.65(a)(2), "Requirements for Monitoring the Effectiveness of Maintenance at
since January 2007. The inspectors  
Nuclear Power Plants," due to FENOC personnel's failure to demonstrate that the  
noted that the Security department  
10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches was  
had generated  
effectively controlled through the performance of appropriate preventive maintenance.  
significantly  
Specifically, as evidenced by repeat dual position indications of containment isolation  
less CRs when compared to the rest of the site. Interviews  
valves in the control room resulting in 21 unplanned entries into Technical Specification  
with Security personnel  
3.6.3, the containment isolation valve system 10 CFR 50.65(a)(2) performance  
revealed that they had received adequate training, displayed  
demonstration was no longer justified in accordance with Maintenance Rule implementing  
a willingness  
procedure guidance.  
to raise issues, and had ample access to computers;  
Description: The containment isolation valve system is a risk-significant system that is  
however, there was a reliance on the shift Captain to enter issues into the CAP. The inspectors  
scoped within the Maintenance Rule because it is a system, structure, or component  
observed managers and supervisors  
(SSC) required to mitigate accidents/transients and is identified in emergency operating  
at MRB meetings appropriately  
procedures. The primary Maintenance Rule function of the containment isolation valve
questioning  
system is to provide a containment isolation function during an event to prevent offsite  
and challenging  
radiological release. Additionally, limit switches associated with each containment  
CRs to ensure clarity of the issues. The inspectors  
isolation valve are scoped within the Maintenance Rule because they provide a function to  
determined  
indicate valve position in the control room for operators to use during emergency  
that FENOC personnel  
operating procedures.  
trended equipment  
In February 2009, during stroke-time testing, an air-operated containment isolation valve
and programmatic  
displayed dual indication in the control room, causing the stroke times of the valve to be  
issues, and CR descriptions  
indeterminate and causing an unplanned entry into Technical Specification 3.6.3.  
appropriately  
Additionally, between January 2007 and July 2009, Technical Specification 3.6.3 had 21  
included reference  
unplanned entries as a result of faulty limit switches on similar containment isolation  
to repeat occurrences  
valves. This resulted in the FENOC established containment isolation valve system  
of issues. The Enclosure   
Maintenance Rule condition monitoring criteria being exceeded, which required FENOC to  
inspectors  
perform a Maintenance Rule 10 CFR 50.65(a)(1) evaluation. The Maintenance Rule
concluded  
(a)(1) evaluation was completed in February 2009 and concluded that the containment  
that personnel  
isolation valve system should continue to be monitored in accordance with Maintenance  
were identifying  
Rule 10 CFR 50.65(a)(2)., This reinforced a similar decision made in 2007 based on a  
trends at low levels. The inspectors  
Maintenance Rule (a)(1) evaluation recommendation to keep the system in (a)(2) despite  
toured plant areas including  
Enclosure  
the turbine buildings, safeguards  
 
buildings, intake structure, emergency  
9  
diesel generator  
the condition monitoring criteria being exceeded due to multiple dual indications in the  
buildings, yard areas, security areas and control room to determine  
control room. The basis of the decision was that the dual indication issue was a result of  
if FENOC personnel  
faulty limit switches, and that this did not affect the valve's safety related function to close  
identified  
during an event to prevent offsite radiological release. Site personnel determined the
plant issues at the proper threshold.  
direct cause was the limit switch being out of adjustment due to a problem with the  
Housekeeping  
required torque. Despite the repeat failures, FENOC failed to implement or revise  
in all areas, with the exception  
preventive maintenance practices for these limit switches. Subsequently, the  
of the Unit 2 intake structure, was noted to be improved since the 2007 NRC PI&R inspection.  
Maintenance Rule Steering Committee approved a revision to clarify the monitoring  
During the plant walkdown, the inspectors  
criteria for the containment isolation valve system, which would exclude future indication  
identified  
problems that did not affect the valve's ability to isolate containment. However, it failed to  
three examples of adverse conditions  
take into account the limit switches' Maintenance Rule function in emergency operating  
that had not been identified  
procedures, specifically, the ability to accurately indicate valve position in the control room  
by FENOC. The following  
during an event. Following the change to the condition monitoring criteria, the site had  
issues were entered into the CAP for evaluation  
seven valves display dual indication in the control room between February 2009 and June  
and resolution: During an inspection  
2009 that FENOC concluded did not affect valve operability.  
of the east end of the main intake structure, the inspectors  
The inspectors concluded that the numerous dual indications of the limit switches should  
identified  
have been evaluated against FENOC's Maintenance Rule condition monitoring criteria
an oxygen bottle strapped to an Appendix R ladder (a ladder used by plant personnel  
and should have resulted in placement of the containment isolation valve system in  
for implementing the  
10 CFR 50.65(a)(1) for goal setting and monitoring. FENOC performed an extent of  
site fire protection  
condition review on two other valves of the same model, and determined that the torque  
program).  
on the limit switch fasteners needed to be adjusted. FENOC corrected the torque issue  
Restraining  
and has implemented plans to install a button tab on the limit switches to minimize  
the oxygen bottle and Appendix R ladder together in this fashion represented  
misalignment causing dual indications.  
a minor procedure  
Analysis: The inspectors determined that the failure to demonstrate that the  
violation  
10 CFR 50.65{a)(2) performance of the containment isolation valve limit switches was  
of Beaver Valley procedure, 1/2-PIP-G01, "Securing  
effectively controlled through the performance of appropriate preventive maintenance was
Transient/Temporary/Stored  
a performance deficiency within FENOC personnel's ability to foresee and correct and  
Equipment  
should have been prevented. Traditional Enforcement did not apply, as the issue did not  
in Safety-Related  
have actual or potential safety consequence, had no willful aspects, nor did it impact the  
Areas." This issue is minor because there was no adverse impact to plant safety equipment, and there was only minimal impact on operator fire response times. FENOC entered this into the CAP (CR 09-63536). During an inspection  
NRC's ability to perform its regulatory function.  
of the 'D' intake structure  
A review of NRC Inspection Manual Chapter (IMC) 0612, Appendix E, "Minor Examples,"  
cubicle, the inspectors  
revealed that no minor examples were applicable to this finding. The inspectors  
identified  
determined the finding was more than minor because it is associated with the Equipment  
rigging scaffolding  
Performance attribute of the Mitigating Systems cornerstone and adversely affected the  
with a chainfall  
cornerstone objective of ensuring the reliability of systems that respond to initiating events
that had been left draped over a safety related component.  
to prevent undesirable consequences. Specifically, the dual indication of containment  
Scaffold contacting  
isolation valves in the control room due to faulty limit switches presents a challenge to the  
plant equipment  
operators during event response while implementing emergency operating procedures,  
represented  
and has resulted in 21 unplanned Technical Specification entries. The numerous dual  
a minor procedure  
indication instances should have caused the containment isolation valve system to be  
violation  
placed in 10 CFR 50.65(a)(1) for goal setting and monitoring. The inspectors determined  
of Beaver Valley procedure, 1/2-ADM-0810, "Scaffold  
the significance of the finding using IMC 0609.04, "Phase 1  
Erection and Tagging." The component  
Initial Screening and
was not damaged nor had any reduced capability  
Characterization of Findings." The finding was determined to be of very low safety  
as a result of the contact with the chainfall.  
significance (Green) because the finding did not involve a design or qualification  
This issue is minor because there was no loss of operability  
deficiency resulting in loss of operability or functionality, did not result in a loss of system  
or adverse impact to the safety related component.  
Enclosure  
FENOC entered this into the CAP (CR 09-63532). During an inspection  
 
of the Unit 2 Safeguards  
10  
Building, the inspectors  
safety function, and did not screen as potentially risk significant due to external initiating  
identified  
events.  
four plastic buckets filled with lubricating  
The inspectors determined that this finding had a cross-cutting aspect in the "Corrective  
oil totaling 20 gallons. The unattended  
Action Program" component of the Problem Identification and Resolution cross-cutting  
oil in a safety related fire area represented  
area because FENOC did not take appropriate corrective actions to address safety issues  
a minor procedure  
and adverse trends associated with faulty containment isolation valve limit switches in a  
violation  
timely manner, commensurate with their safety significance and complexity [P.1 (d)).  
of Beaver Valley procedure, 1/2-ADM-1906, "Control of Transient  
Enforcement: 10 CFR 50.65(a)(1) requires, in part, that holders of an operating license
Combustible  
shall monitor the performance or condition of SSCs within the scope of the monitoring  
and Flammable  
program as defined in 10 CFR 50.65(b) against licensee-established goals, in a manner  
Materials." This issue is minor because the increase in combustible  
sufficient to provide reasonable assurance that such SSCs are capable of fulfilling their
loading in the room as a result of the unattended  
intended functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in
oil did not violate the plant fire hazard analysis.  
10 CFR 50.65(a)(1) is not required where it has been demonstrated that the performance  
FENOC entered this into the CAP (CR 09-63441).  
or condition of an SSC is being effectively controlled through the performance of
In accordance  
appropriate preventative maintenance, such that the SSC remains capable of performing  
with NRC Inspection  
Manual Chapter 0612, "Power Reactor Inspection  
Reports," the above issues constitute  
violations  
of minor significance  
that are not subject to enforcement  
action in accordance  
with the NRC's Enforcement  
Policy. Effectiveness  
of Prioritization  
and Evaluation  
of Issues The inspectors  
determined  
that, in general, FENOC personnel  
appropriately  
prioritized  
and evaluated  
issues commensurate  
with their safety significance.  
CRs were screened for operability  
and reportability, categorized  
by significance, and assigned to a department  
for evaluation  
and resolution.  
The CR screening  
process considered  
human performance  
issues, radiological  
safety concerns, repetitiveness  
and adverse trends. The inspectors  
observed managers and supervisors  
at MRB meetings appropriately  
questioning  
and challenging  
CRs to ensure appropriate  
prioritization.  
Enclosure   
CRs were categorized  
for evaluation  
and resolution  
commensurate  
with the significance  
of the issues. Based on the sample of CRs reviewed, the guidance provided by the FENOC implementing procedures appeared  
sufficient  
to ensure consistency  
in categorization  
of the issues. Operability  
and reportability  
determinations  
were performed  
when conditions  
warranted  
and the evaluations  
supported  
the conclusions.  
Causal analyses appropriately  
considered  
extent of condition, generic issues, and previous occurrences.  
During this inspection, the inspectors  
noted that, in general, FENOC's root cause analyses were thorough, and corrective  
and preventive  
actions addressed  
the identified  
causes. Additionally, the identified  
causes were well supported.  
An NCV was identified  
for FENOC's failure to demonstrate  
that the 10 CFR 50.65(a)(2)  
performance  
of the containment  
isolation  
valve limit switches was effectively  
controlled  
through the performance  
of appropriate  
preventive  
maintenance.  
This NCV is discussed  
in the findings section of this assessment  
area. The inspectors  
identified  
the following  
two examples of issues that were not fully evaluated  
or prioritized  
for corrective  
action: A root cause evaluation (CR 08-39835)  
associated  
with a 2.5 inch drain down of the Unit 2 reactor coolant system during refueling  
outage 2R13 did not identify all corrective  
actions necessary  
to address all failed barriers.  
The inspectors  
noted that the root cause evaluation  
had not included corrective  
actions to address the communication  
failure within operations  
shifts, and the work management  
scheduling  
issues which contributed  
to a component  
tagoutlctearance  
being inappropriately  
implemented.  
The issue is minor because while corrective  
actions were not assigned to address all failed barriers, FENOC had discussed  
communication  
expectations  
with each operating  
crew and there have not been any repeat issues. FENOC entered these issues into the CAP (CR 09-63454 and 09-63479). The inspectors  
identified  
three CRs describing  
component  
mispositioning  
events (CR 09-59541, CR 09-58355, and CR 09-57224)  
that were prioritized  
as CR level OlAF." The failure to prioritize  
these CRs as a limited apparent cause (CR level "AL") represented  
a minor procedure  
violation  
of Beaver Valley procedure, OP-0004, "Component  
Mispositioning." The inspectors  
reviewed NRC Inspection  
Manual Chapter 0612, Appendix E, "Minor Examples," and determined  
this issue was minor because there  
was no loss of operability  
or safety impact. FENOC entered this issue into the CAP (CR 09-64004 and CR 09-63975).  
In accordance  
with NRC Inspection  
Manual Chapter 0612, "Power Reactor Inspection  
Reports," these issues constitute  
violations  
of minor significance  
that are not subject to enforcement  
action in accordance  
with the NRC's Enforcement  
Policy. Effectiveness  
of Corrective  
Actions The inspectors  
concluded  
that corrective  
actions for identified  
deficiencies  
were generally  
timely and adequately  
implemented.  
For significant  
conditions  
adverse to quality, corrective  
actions were identified  
to prevent recurrence.  
The inspectors  
concluded  
that corrective  
actions to address NCVs and findings since the last PI&R inspection  
were timely and effective.  
The inspectors  
identified  
the following  
example where corrective  
actions were not fully effective  
in addressing  
an issue: Enclosure   
The inspectors  
reviewed corrective  
actions taken in response to an NCV documented  
in NRC report 05000334/05000412  
2007004. CR 07-24074 was written to ensure bearing temperatures  
would be monitored  
when performing  
surveillance  
testing on the turbine driven auxiliary  
feedpumps (TDAFWP).  
The inspectors  
found that the comprehensive  
surveillance  
tests for Unit 1 and Unit 2 (Beaver Valley procedures  
10ST-24.9  
and 20ST-24.4A, respectively)  
did not have a precaution  
stating that this surveillance  
was not suitable to be used for post maintenance  
testing as there is no guidance prescribed  
to monitor and achieve steady bearing temperatures.  
The inspectors  
determined  
that the issue was minor because the preventive  
maintenance  
work order had contained  
the appropriate  
guidance.  
FENOC entered this issue into the CAP (CR 09-64015).  
c. Findings Introduction:  
The inspectors  
identified  
an NCV of very low safety significance (Green) of 10 CFR 50.65(a)(2), "Requirements  
for Monitoring  
the Effectiveness  
of Maintenance  
at Nuclear Power Plants," due to FENOC personnel's  
failure to demonstrate  
that the 10 CFR 50.65(a)(2)  
performance  
of the containment  
isolation  
valve limit switches was effectively  
controlled  
through the performance  
of appropriate  
preventive  
maintenance.  
Specifically, as evidenced  
by repeat dual position indications  
of containment  
isolation  
valves in the control room resulting  
in 21 unplanned entries into  
Technical  
Specification  
3.6.3, the containment  
isolation  
valve system 10 CFR 50.65(a)(2)  
performance  
demonstration  
was no longer justified  
in accordance  
with Maintenance  
Rule implementing  
procedure  
guidance.  
Description:  
The containment  
isolation  
valve system is a risk-significant  
system that is scoped within the Maintenance  
Rule because it is a system, structure, or component (SSC) required to mitigate accidents/transients  
and is identified  
in emergency  
operating  
procedures.  
The primary Maintenance  
Rule function of the containment  
isolation  
valve system is to provide a containment  
isolation  
function during an event to prevent offsite radiological  
release. Additionally, limit switches associated  
with each containment  
isolation  
valve are scoped within the Maintenance  
Rule because they provide a function to indicate valve position  
in the control room for operators  
to use during emergency  
operating  
procedures.  
In February 2009, during stroke-time  
testing, an air-operated  
containment  
isolation  
valve displayed  
dual indication  
in the control room, causing the stroke times of the valve to be indeterminate  
and causing an unplanned  
entry into Technical  
Specification  
3.6.3. Additionally, between January 2007 and July 2009, Technical  
Specification  
3.6.3 had 21 unplanned  
entries as a result of faulty limit switches on similar containment  
isolation  
valves. This resulted in the FENOC established  
containment  
isolation  
valve system Maintenance  
Rule condition  
monitoring  
criteria being exceeded, which required FENOC to perform a Maintenance  
Rule 10 CFR 50.65(a)(1)  
evaluation.  
The Maintenance  
Rule (a)(1) evaluation  
was completed  
in February 2009 and concluded  
that the containment  
isolation  
valve system should continue to be monitored  
in accordance  
with Maintenance  
Rule 10 CFR 50.65(a)(2)., This reinforced  
a similar decision made in 2007 based on a Maintenance  
Rule (a)(1) evaluation  
recommendation  
to keep the system in (a)(2) despite Enclosure   
the condition  
monitoring  
criteria being exceeded due to multiple dual indications  
in the control room. The basis of the decision was that the dual indication  
issue was a result of faulty limit switches, and that this did not affect the valve's safety related function to close during an event to prevent offsite radiological  
release. Site personnel  
determined  
the direct cause was the limit switch being out of adjustment  
due to a problem with the required torque. Despite the repeat failures, FENOC failed to implement  
or revise preventive  
maintenance  
practices  
for these limit switches.  
Subsequently, the Maintenance  
Rule Steering Committee  
approved a revision to clarify the monitoring  
criteria for the containment  
isolation  
valve system, which would exclude future indication  
problems that did not affect the valve's ability to isolate containment.  
However, it failed to take into account the limit switches'  
Maintenance  
Rule function in emergency  
operating  
procedures, specifically, the ability to accurately  
indicate valve position in the control room during an event. Following  
the change to the condition  
monitoring  
criteria, the site had seven valves display dual indication  
in the control room between February 2009 and June 2009 that FENOC concluded  
did not affect valve operability.  
The inspectors  
concluded  
that the numerous dual indications  
of the limit switches should have been evaluated  
against FENOC's Maintenance  
Rule condition  
monitoring  
criteria and should have resulted in placement  
of the containment  
isolation  
valve system in 10 CFR 50.65(a)(1)  
for goal setting and monitoring.  
FENOC performed  
an extent of condition  
review on two other valves of the same model, and determined  
that the torque on the limit switch fasteners  
needed to be adjusted.  
FENOC corrected  
the torque issue and has implemented  
plans to install a button tab on the limit switches to minimize misalignment  
causing dual indications.  
Analysis:  
The inspectors  
determined  
that the failure to demonstrate  
that the 10 CFR 50.65{a)(2)  
performance  
of the containment  
isolation  
valve limit switches was effectively  
controlled  
through the performance  
of appropriate  
preventive  
maintenance  
was a performance  
deficiency  
within FENOC personnel's  
ability to foresee and correct and should have been prevented.  
Traditional  
Enforcement  
did not apply, as the issue did not have actual or potential  
safety consequence, had no willful aspects, nor did it impact the NRC's ability to perform its regulatory  
function.  
A review of NRC Inspection  
Manual Chapter (IMC) 0612, Appendix E, "Minor Examples," revealed that no minor examples were applicable  
to this finding. The inspectors  
determined  
the finding was more than minor because it is associated  
with the Equipment  
Performance  
attribute  
of the Mitigating  
Systems cornerstone  
and adversely  
affected the cornerstone  
objective  
of ensuring the reliability  
of systems that respond to initiating  
events to prevent undesirable  
consequences.  
Specifically, the dual indication  
of containment  
isolation  
valves in the control room due to faulty limit switches presents a challenge  
to the operators  
during event response while implementing  
emergency  
operating  
procedures, and has resulted in 21 unplanned  
Technical  
Specification  
entries. The numerous dual indication  
instances  
should have caused the containment  
isolation  
valve system to be placed in 10 CFR 50.65(a)(1)  
for goal setting and monitoring.  
The inspectors  
determined  
the significance  
of the finding using IMC 0609.04, "Phase 1 Initial Screening  
and Characterization  
of Findings." The finding was determined  
to be of very low safety significance (Green) because the finding did not involve a design or qualification  
deficiency  
resulting  
in loss of operability  
or functionality, did not result in a loss of system Enclosure   
safety function, and did not screen as potentially  
risk significant  
due to external initiating  
events. The inspectors  
determined  
that this finding had a cross-cutting  
aspect in the "Corrective  
Action Program" component  
of the Problem Identification  
and Resolution  
cross-cutting  
area because FENOC did not take appropriate  
corrective  
actions to address safety issues and adverse trends associated  
with faulty containment  
isolation  
valve limit switches in a timely manner, commensurate  
with their safety  
significance  
and complexity  
[P.1 (d)). Enforcement:  
10 CFR 50.65(a)(1)  
requires, in part, that holders of an operating  
license shall monitor the performance  
or condition  
of SSCs within the scope of the monitoring  
program as defined in 10 CFR 50.65(b) against licensee-established  
goals, in a manner sufficient  
to provide reasonable  
assurance  
that such SSCs are capable of fulfilling  
their intended functions.  
10 CFR 50.65(a)(2)  
states, in part, that monitoring  
as specified  
in 10 CFR 50.65(a)(1)  
is not required where it has been demonstrated  
that the performance  
or condition  
of an SSC is being effectively  
controlled  
through the performance  
of appropriate  
preventative  
maintenance, such that the SSC remains capable of performing  
its intended function.  
its intended function.  
Contrary to the above, between 2007 and 2009, FENOC personnel  
Contrary to the above, between 2007 and 2009, FENOC personnel failed to demonstrate  
failed to demonstrate  
that the 10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches  
that the 10 CFR 50.65(a)(2)  
was effectively controlled through the performance of appropriate preventive  
performance  
maintenance. FENOC has performed an extent of condition review and has initiated  
of the containment  
corrective actions to install a button tab on the limit switches to minimize misalignment  
isolation  
causing the dual indications. Because this violation was of very low safety significance  
valve limit switches was effectively  
and has been entered into the CAP (CR 09-64040), this violation is being treated as an  
controlled  
NCV, consistent with the NRC Enforcement Policy (NCV 05000314,412/2009008-01:  
through the performance  
Containment Isolation Valve System 10 CFR 50.65 (a)(2) Performance  
of appropriate  
Demonstration Not Met) .  
preventive  
. 2  
maintenance.  
Assessment of the Use of Operating Experience  
FENOC has performed  
a.  
an extent of condition  
Inspection Scope
review and has initiated  
The inspectors selected a sample of CRs associated with the review of industry Operating  
corrective  
Experience (OE) to determine whether FENOC personnel appropriately evaluated the OE  
actions to install a button tab on the limit switches to minimize misalignment  
information for applicability to Beaver Valley and had taken appropriate actions, when  
causing the dual indications.  
warranted. The inspectors reviewed CR evaluations of OE documents associated with a  
Because this violation  
sample of NRC Generic Letters and Information Notices to ensure that FENOC  
was of very low safety significance  
adequately considered the underlying problems associated with the issues for resolution  
and has been entered into the CAP (CR 09-64040), this violation  
via their CAP. The inspectors also observed plant activities to determine if industry OE  
is being treated as an NCV, consistent  
was considered during the performance of routine activities. Specific documents  
with the NRC Enforcement  
reviewed during the inspection are listed in the Attachment to this report.  
Policy (NCV 05000314,412/2009008-01:  
b.  
Containment  
Assessment  
Isolation  
The inspectors determined that, in general, FENOC appropriately considered industry OE  
Valve System 10 CFR 50.65 (a)(2) Performance  
information for applicability, and used the information for corrective and preventive actions
Demonstration  
Enclosure  
Not Met) . . 2 Assessment  
 
of the Use of Operating  
11  
Experience  
to identify and prevent similar issues when appropriate. The inspectors determined that
a. Inspection  
OE was appropriately applied and lessons learned were communicated and incorporated  
Scope The inspectors  
into plant operations. The inspectors observed that industry OE was routinely discussed  
selected a sample of CRs associated  
and considered during the performance of plant activities.  
with the review of industry Operating  
The inspectors reviewed a fleet-level focused self-assessment of OE performed in May  
Experience (OE) to determine  
2008. The self-assessment identified a number of weaknesses, specifically:  
whether FENOC personnel  
OE was not discussed in system health reports;  
appropriately  
Roles and responsibilities of Section OE Coordinators were not clearly defined;  
evaluated  
the OE information  
Familiarization with SAP, the database used to manage OE, was low at the  
for applicability  
Management and Section OE Coordinator levels; and  
to Beaver Valley and had taken appropriate  
Procedures describing the requirements to process OE were in need of revision to  
actions, when warranted.  
add clarity.  
The inspectors  
Although the inspectors noted that corrective actions were not completed until June 2009,  
reviewed CR evaluations  
since that time Beaver Valley has made progress in addressing OE program needs. This  
of OE documents  
has included clearly defining the roles and responsibilities of Section OE Coordinators.  
associated  
Procedures have been revised and a familiarization guide has been completed with
with a sample of NRC Generic Letters and Information  
guidance on how to use SAP efficiently. Training has been completed for Section OE  
Notices to ensure that FENOC adequately  
Coordinators and the backlog of unreviewed OE items has decreased (currently at 2  
considered  
unreviewed items as compared to over 12 items previously). Finally, a higher level of  
the underlying  
accountability has been placed on each department to report backlogged OE items at  
problems associated  
weekly plant meetings. With respect to incorporating OE in system health reports, the  
with the issues for resolution  
inspectors identified that OE continued not to be incorporated in the 2008 and 2009  
via their CAP. The inspectors  
reports. FENOC entered this issue into the CAP (CR 09-63999).  
also observed plant activities  
c.  
to determine  
Findings  
if industry OE was considered  
No findings of significance were identified .  
during the performance  
. 3  
of routine activities.  
Assessment of Self-Assessments and Audits  
Specific documents  
a.  
reviewed during the inspection  
Inspection Scope
are listed in the Attachment  
The inspectors reviewed a sample of snapshot self-assessments, focused self
to this report. b. Assessment  
assessments, fleet-level assessments, and a variety of self-assessments focused on  
The inspectors  
various plant programs. These reviews were performed to determine if problems  
determined  
identified through these assessments were entered into the CAP, and whether corrective  
that, in general, FENOC appropriately  
actions were initiated to address identified deficiencies. The effectiveness of the  
considered  
assessments was evaluated by comparing audit and assessment results against  
industry OE information  
self-revealing and NRC-identified observations made during the inspection. A list of  
for applicability, and used the information  
documents reviewed is included in the Attachment to this report.  
for corrective  
b.  
and preventive  
Assessment  
actions Enclosure   
The inspectors concluded that QA audits and self-assessments were critical, thorough,  
to identify and prevent similar issues when appropriate.  
and effective in identifying issues. The inspectors observed that these audits and self-
The inspectors  
Enclosure  
determined  
 
that OE was appropriately  
.4  
applied and lessons learned were communicated  
12  
and incorporated  
assessments were completed by personnel knowledgeable in the subject areas and were  
into plant operations.  
completed to a sufficient depth to identify issues that were then entered into the CAP for  
The inspectors  
evaluation. Corrective actions associated with the issues were implemented  
observed that industry OE was routinely  
commensurate with their safety significance. FENOC managers evaluated the results and  
discussed  
initiated appropriate actions to focus on areas identified for improvement.  
and considered  
c.  
during the performance  
Findings  
of plant activities.  
No findings of significance were identified .  
The inspectors  
Assessment of Safety Conscious Work Environment  
reviewed a fleet-level  
a.  
focused self-assessment  
Inspection Scope
of OE performed  
The inspectors performed interviews with station personnel to assess the safety conscious  
in May 2008. The self-assessment  
work environment (SCWE) at Beaver Valley. Specifically, the inspectors interviewed  
identified  
personnel to determine whether they were hesitant to raise safety concerns to their  
a number of weaknesses, specifically: OE was not discussed  
management and/or the NRC. The inspectors also interviewed the station Employee  
in system health reports; Roles and responsibilities  
Concerns Program (ECP) coordinator to determine what actions were implemented to
of Section OE Coordinators  
ensure employees were aware of the program and its availability with regard to raising  
were not clearly defined; Familiarization  
concerns. The inspectors reviewed the ECP files to ensure that issues were entered into  
with SAP, the database used to manage OE, was low at the Management  
the CAP when appropriate. The inspectors reviewed site SCWE surveys from 2007 and  
and Section OE Coordinator  
2008 to assess any adverse trends in department and site safety culture. A list of  
levels; and Procedures  
documents reviewed is included in the Attachment to this report.  
describing  
b.  
the requirements  
Assessment  
to process OE were in need of revision to add clarity. Although the inspectors  
During interviews, plant staff expressed a willingness to use the CAP to identify plant  
noted that corrective  
issues and deficiencies, and stated that they were willing to raise safety issues. All  
actions were not completed  
persons interviewed demonstrated an adequate knowledge of the CAP and ECP. Based  
until June 2009, since that time Beaver Valley has made progress in addressing  
on these limited interviews, the inspectors concluded that there was no evidence of  
OE program needs. This has included clearly defining the roles and responsibilities  
SCWE concerns and no significant challenges to the free flow of information.  
of Section OE Coordinators.  
SCWE surveys in 2007 and 2008 showed that the overall SCWE health at Beaver Valley  
Procedures  
remained positive. The surveys indicated the staff understands and accepts expectations  
have been revised and a familiarization  
and responsibilities for identifying concerns. The surveys indicated FENOC personnel  
guide has been completed  
feel free to approach management with issues and management expectations on safety  
with guidance on how to use SAP efficiently.  
and quality are clearly communicated. The surveys indicated lower than average scores  
Training has been completed  
for Radiation Protection, Chemistry, Security, and Site Projects departments. CRs were  
for Section OE Coordinators  
generated to help promote improvement in the safety culture of these departments, and  
and the backlog of unreviewed  
corrective actions were implemented. The inspectors noted that when compared to the  
OE items has decreased (currently  
2007 survey, the Operations department had an increase in negative responses in the  
at 2 unreviewed  
2008 survey. This trend had not been entered into the CAP for evaluation since the  
items as compared to over 12 items previously).  
negative score averages did not exceed a ten percent cutoff "trigger" for CR generation.  
Finally, a higher level of accountability  
The inspectors questioned this cutoff in that it appeared to potentially limit FENOC's ability  
has been placed on each department  
to fully explore year-to-year trends in departments that may not exceed ten percent  
to report backlogged  
negative responses, but decline significantly from the previous survey_ FENOC entered  
OE items at weekly plant meetings.  
this issue into the CAP (CR 09-63998).  
With respect to incorporating  
Enclosure  
OE in system health reports, the inspectors  
 
identified  
13  
that OE continued  
As a result of the survey review, the inspectors completed additional SCWE interviews  
not to be incorporated  
with operators to determine if there was a reluctance to raise safety issues. No individuals  
in the 2008 and 2009 reports. FENOC entered this issue into the CAP (CR 09-63999).  
expressed any fear to raise issues.  
c. Findings No findings of significance  
c. 
were identified . . 3 Assessment  
Findings
of Self-Assessments  
No findings of significance were identified.  
and Audits a. Inspection  
40A6 Meetings, Including Exit
Scope The inspectors  
On September 3, 2009, the inspectors presented the inspection results to Mr. Roy Brosi,  
reviewed a sample of snapshot self-assessments, focused assessments, fleet-level  
Director of Site Performance Improvement, and other members of the Beaver Valley staff.  
assessments, and a variety of self-assessments  
The inspectors verified that no proprietary information was documented in the report.  
focused on various plant programs.  
ATTACHMENT: SUPPLEMENTAL INFORMATION  
These reviews were performed  
Enclosure  
to determine  
 
if problems identified  
A-1  
through these assessments  
SUPPLEMENTAL INFORMATION 
were entered into the CAP, and whether corrective  
KEY POINTS OF CONTACT 
actions were initiated  
Licensee personnel  
to address identified  
deficiencies.  
The effectiveness  
of the assessments  
was evaluated  
by comparing  
audit and assessment  
results against self-revealing  
and NRC-identified  
observations  
made during the inspection.  
A list of documents  
reviewed is included in the Attachment  
to this report. b. Assessment  
The inspectors  
concluded  
that QA audits and self-assessments  
were critical, thorough, and effective  
in identifying  
issues. The inspectors  
observed that these audits and self-Enclosure
.4 12 assessments  
were completed  
by personnel  
knowledgeable  
in the subject areas and were completed  
to a sufficient  
depth to identify issues that were then entered into the CAP for evaluation.  
Corrective  
actions associated  
with the issues were implemented  
commensurate  
with their safety significance.  
FENOC managers evaluated  
the results and initiated  
appropriate  
actions to focus on areas identified  
for improvement.  
c. Findings No findings of significance  
were identified . Assessment  
of Safety Conscious  
Work Environment  
a. Inspection  
Scope The inspectors  
performed  
interviews  
with station personnel  
to assess the safety conscious  
work environment (SCWE) at Beaver Valley. Specifically, the inspectors  
interviewed  
personnel  
to determine  
whether they were hesitant to raise safety concerns to their management  
and/or the NRC. The inspectors  
also interviewed  
the station Employee Concerns Program (ECP) coordinator  
to determine  
what actions were implemented  
to ensure employees  
were aware of the program and its availability  
with regard to raising concerns.  
The inspectors  
reviewed the ECP files to ensure that issues were entered into the CAP when appropriate.  
The inspectors  
reviewed site SCWE surveys from 2007 and 2008 to assess any adverse trends in department  
and site safety culture. A list of documents  
reviewed is included in the Attachment  
to this report. b. Assessment  
During interviews, plant staff expressed  
a willingness  
to use the CAP to identify plant issues and deficiencies, and stated that they were willing to raise safety issues. All persons interviewed  
demonstrated  
an adequate knowledge  
of the CAP and ECP. Based on these limited interviews, the inspectors  
concluded  
that there was no evidence of SCWE concerns and no significant  
challenges  
to the free flow of information.  
SCWE surveys in 2007 and 2008 showed that the overall SCWE health at Beaver Valley remained positive.  
The surveys indicated  
the staff understands  
and accepts expectations  
and responsibilities  
for identifying  
concerns.  
The surveys indicated  
FENOC personnel  
feel free to approach management  
with issues and management  
expectations  
on safety and quality are clearly communicated.  
The surveys indicated  
lower than average scores for Radiation  
Protection, Chemistry, Security, and Site Projects departments.  
CRs were generated  
to help promote improvement  
in the safety culture of these departments, and corrective  
actions were implemented.  
The inspectors  
noted that when compared to the 2007 survey, the Operations  
department  
had an increase in negative responses  
in the 2008 survey. This trend had not been entered into the CAP for evaluation  
since the negative score averages did not exceed a ten percent cutoff "trigger" for CR generation.  
The inspectors  
questioned  
this cutoff in that it appeared to potentially  
limit FENOC's ability to fully explore year-to-year  
trends in departments  
that may not exceed ten percent negative responses, but decline significantly  
from the previous survey_ FENOC entered this issue into the CAP (CR 09-63998).  
Enclosure   
As a result of the survey review, the inspectors  
completed  
additional  
SCWE interviews  
with operators  
to determine  
if there was a reluctance  
to raise safety issues. No individuals  
expressed  
any fear to raise issues. Findings No findings of significance  
were identified.  
40A6 Meetings, Including  
Exit On September  
3, 2009, the inspectors  
presented  
the inspection  
results to Mr. Roy Brosi, Director of Site Performance  
Improvement, and other members of the Beaver Valley staff. The inspectors  
verified that no proprietary  
information  
was documented  
in the report. ATTACHMENT:  
SUPPLEMENTAL  
INFORMATION  
Enclosure
A-1 SUPPLEMENTAL  
KEY POINTS OF Licensee personnel  
Harold Szklinski, Staff Nuclear Specialist  
Harold Szklinski, Staff Nuclear Specialist  
Fulton Schaffner, Staff Nuclear Specialist  
Fulton Schaffner, Staff Nuclear Specialist  
Daniel Butor, Staff Nuclear Specialist  
Daniel Butor, Staff Nuclear Specialist  
Robert Lubert, Supervisor, Nuclear Electrical  
Robert Lubert, Supervisor, Nuclear Electrical System Engineering  
System Engineering  
Francy Mantine, Staff Nuclear Engineer  
Francy Mantine, Staff Nuclear Engineer David Jones, Staff Nuclear Engineer Philip Slifkin, Staff Nuclear Engineer Giuseppe Cerasi, Senior Nuclear Specialist  
David Jones, Staff Nuclear Engineer  
Brian Goff, Supervisor, Nuclear Work Planning Michael Kienzle, Nuclear Engineering  
Philip Slifkin, Staff Nuclear Engineer  
Giuseppe Cerasi, Senior Nuclear Specialist  
Brian Goff, Supervisor, Nuclear Work Planning  
Michael Kienzle, Nuclear Engineering  
Pat Pauvlinch, Supervisor, Nuclear Plant System Engineering  
Pat Pauvlinch, Supervisor, Nuclear Plant System Engineering  
Robert Williams, Staff Nuclear Engineer Joann West, Staff Nuclear Engineer John Kaminskas, Nuclear Engineer David Hauser, Superintendent  
Robert Williams, Staff Nuclear Engineer  
Shift Operations, Unit 2 Christopher  
Joann West, Staff Nuclear Engineer  
Makowka, Root Cause Evaluator  
John Kaminskas, Nuclear Engineer  
Michael Mitchell, Superintendent  
David Hauser, Superintendent Shift Operations, Unit 2  
Nuclear Work Planning John Bowden, Superintendent  
Christopher Makowka, Root Cause Evaluator  
Nuclear Operations  
Michael Mitchell, Superintendent Nuclear Work Planning  
Services Jim Mauck, Senior Nuclear Specialist  
John Bowden, Superintendent Nuclear Operations Services
Jim Mauck, Senior Nuclear Specialist  
Brian Sepelak, Supervisor, Nuclear Compliance  
Brian Sepelak, Supervisor, Nuclear Compliance  
Karl Wolfson, Supervisor, Nuclear Performance  
Karl Wolfson, Supervisor, Nuclear Performance Improvement  
Improvement  
Colin Keller, Manager, Site Regulatory Compliance  
Colin Keller, Manager, Site Regulatory  
Compliance  
Rich Dibler, Security Support Supervisor  
Rich Dibler, Security Support Supervisor  
Sue Vincinie, Performance  
Sue Vincinie, Performance Improvement Senior Consultant  
Improvement  
Senior Consultant  
Darrel Batina, Employee Concerns Program Representative  
Darrel Batina, Employee Concerns Program Representative  
Dutch Chancey, Manager, Employee Concerns (Fleet) Wayne Mcintire, Beaver Valley Site Safety Specialist  
Dutch Chancey, Manager, Employee Concerns (Fleet)  
Wayne Mcintire, Beaver Valley Site Safety Specialist  
Gary Shildt, Supervisor, Nuclear Projects Engineering  
Gary Shildt, Supervisor, Nuclear Projects Engineering  
Jack Patterson, Staff Nuclear Engineer Thomas King, Plant Engineer Robert Lubert, Plant  
Jack Patterson, Staff Nuclear Engineer  
Engineering  
Thomas King, Plant Engineer  
Supervisor  
Robert Lubert, Plant Engineering Supervisor  
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED  
Opened and Closed 05000334, 412/2009008-01  
Opened and Closed  
Containment  
05000334, 412/2009008-01  
Isolation  
Containment Isolation Valve System 10 CFR 50.65  
Valve System 10 CFR 50.65 (a)(2) Performance  
(a)(2) Performance Demonstration Not Met.  
Demonstration  
Attachment  
Not Met. Attachment   
 
LIST OF DOCUMENTS  
A-2  
Condition  
LIST OF DOCUMENTS REVIEWED 
ReQorts 08-38146 09-60763 09-55789 08-50881 08-47439 08-46291 08-45288 08-42054 08-36772 07-26862 08-32856 07-14885  
Condition ReQorts
07-14208 09-62156 09-62106 09-61128 09-60432  
08-38146  
09-59875 09-56773 09-54230  
09-60763  
09-52736 08-39941 08-48160 09-57390  
09-55789  
09-52275 08-49681 08-33109 07-28371 07-15761 09-61333 08-42790 09-62268  
08-50881  
09-59641 09-58307 09-57580 09-57463  
08-47439  
09-55267 09-52029 08-48296 09-57822 09-61026 09-60359 09-56525 09-61753 09-57743 08-51000 07-23937 09-59057 09-53803 08-41802  
08-46291  
08-32965 03-01371 09-61679 09-62681 09-57726 08-39835 07-18191 07-21962 08-48581 08-50283 09-52719 09-61026 09-63451 09-61453 08-48268 08-44941 08-44947 08-37921 08-44960 07-24074 07-30275 09-63317  
08-45288  
08-48482 09-52857 09-63269 09-57857 09-56402  
08-42054  
08-34526 08-33776 09-55350 09-52043 07-28809 07-12360  
08-36772  
07-14181 07-14185 07-14530  
07-26862  
07-14761 07-14934 09-61430 09-61631 09-61878 09-62202 09-62810 07-15636 07-17006 07-17236 07-20147 07-20158  
08-32856  
07-22189 07-24552 07-25283 07-28203  
07-14885  
07-22004 07-29608 07-30073 09-57198  
07-14208  
09-57688 09-57815 09-58598 09-60492 09-60672 09-59088 09-60547 09-61017  
09-62156  
07-31483 07-28809 07-12120 08-35376 08-49694 08-43202  
09-62106  
08-43205 09-62787 08-48664  
09-61128  
08-49518 09-53081 09-53243 09-53762 09-54051 09-55146 09-55719 09-56851 09-56874 09-57268 09-57784 09-58142  
09-60432  
07-26688 09-54051 08-48664 07-25046 07-30273 08-38146 07-13076  
09-59875  
08-48581 09-60218 04-09895 07-30390 07-32095 08-40472 08-48688 09-60450  
09-56773  
06-11217 07-30430 08-32447  
09-54230  
08-40490 08-49073 09-60763 07-13021 07-30431 08-32887 08-40519  
09-52736  
08-49368 09-61744 07-15001 07-30447 08-33126 08-40575  
08-39941  
08-49750 09-62348 07-15444 07-30484 08-33306 08-40579 08-49983 09-62705  
08-48160  
07-18894 07-30575 08-33398 08-40587 08-50137 08-37743  
09-57390  
07-20907 07-30677 08-33725 08-40753  
09-52275  
08-50151 08-37925 07-22891 07-30823 08-35048 08-40867 08-51024 08-38276 07-23543 07-30847 08-35517 08-40932 08-51136 08-38687  
08-49681  
07-23933 07-30911 08-35674 08-40970 08-51385 08-38750  
08-33109  
07-26020 07-30912 08-36383 08-41330 09-52096  
07-28371  
08-39233 Attachment   
07-15761  
07-26065 07-30988 08-36471 08-41450 09-52351  
09-61333  
07-26326 07-30999 08-36539  
08-42790  
08-41691 09-53214 07-27423 07-31040 08-37026 08-41723 09-53275  
09-62268  
07-27469 07-31083 08-37250  
09-59641  
08-41801 09-53803 07-28007 07-31107 08-37304 08-42046 09-53938 07-28012 07-31110 08-37318 08-42627  
09-58307  
09-57580  
09-57463  
09-55267  
09-52029  
08-48296  
09-57822  
09-61026  
09-60359  
09-56525  
09-61753  
09-57743  
08-51000  
07-23937  
09-59057  
09-53803  
08-41802  
08-32965  
03-01371  
09-61679  
09-62681  
09-57726  
08-39835  
07-18191  
07-21962  
08-48581  
08-50283  
09-52719  
09-61026  
09-63451  
09-61453  
08-48268  
08-44941  
08-44947  
08-37921  
08-44960  
07-24074  
07-30275  
09-63317  
08-48482  
09-52857  
09-63269  
09-57857  
09-56402  
08-34526  
08-33776  
09-55350  
09-52043  
07-28809  
07-12360  
07-14181  
07-14185  
07-14530  
07-14761  
07-14934  
09-61430  
09-61631  
09-61878  
09-62202  
09-62810  
07-15636  
07-17006  
07-17236  
07-20147  
07-20158  
07-22189  
07-24552  
07-25283  
07-28203  
07-22004  
07-29608  
07-30073  
09-57198  
09-57688  
09-57815  
09-58598  
09-60492  
09-60672  
09-59088  
09-60547  
09-61017  
07-31483  
07-28809  
07-12120  
08-35376  
08-49694  
08-43202  
08-43205  
09-62787  
08-48664  
08-49518  
09-53081  
09-53243  
09-53762  
09-54051  
09-55146  
09-55719  
09-56851  
09-56874  
09-57268  
09-57784  
09-58142  
07-26688  
09-54051  
08-48664  
07-25046  
07-30273  
08-38146  
07-13076  
08-48581  
09-60218  
04-09895  
07-30390  
07-32095  
08-40472  
08-48688  
09-60450  
06-11217  
07-30430  
08-32447  
08-40490  
08-49073  
09-60763  
07-13021  
07-30431  
08-32887  
08-40519  
08-49368  
09-61744  
07-15001  
07-30447  
08-33126  
08-40575  
08-49750  
09-62348  
07-15444  
07-30484  
08-33306  
08-40579  
08-49983  
09-62705  
07-18894  
07-30575  
08-33398  
08-40587  
08-50137  
08-37743  
07-20907  
07-30677  
08-33725  
08-40753  
08-50151  
08-37925  
07-22891  
07-30823  
08-35048  
08-40867  
08-51024  
08-38276  
07-23543  
07-30847  
08-35517  
08-40932  
08-51136  
08-38687  
07-23933  
07-30911  
08-35674  
08-40970  
08-51385  
08-38750  
07-26020  
07-30912  
08-36383  
08-41330  
09-52096  
08-39233  
Attachment  
 
A-3  
07-26065  
07-30988  
08-36471  
08-41450  
09-52351  
08-39304 
07-26326  
07-30999  
08-36539  
08-41691  
09-53214  
08-39946 
07-27423  
07-31040  
08-37026  
08-41723  
09-53275  
08-46995 
07-27469  
07-31083  
08-37250  
08-41801  
09-53803  
08-47282 
07-28007  
07-31107  
08-37304  
08-42046  
09-53938  
08-47455 
07-28012  
07-31110  
08-37318  
08-42627  
09-54227  
09-54227  
07-28471 07-31112 08-37320 08-42847 09-54737  
08-47767 
07-28724 07-31221 08-37330 08-43510 09-54836 07-29217 07-31350 08-37373 08-44047  
07-28471  
09-55439 07-30075 07-30383 08-37405 08-45833 09-56328  
07-31112  
07-30318 08-37676 08-37450 08-46143 09-57224 07-30362 08-46883 08-37646 08-46662  
08-37320  
09-57244 07-28652 08-38049 08-41776 08-47368 08-47539 09-53197 09-53372 09-53569 09-55916 09-57165 07-16667 07-17938 07-19218 07-20942  
08-42847  
07-23163 07-24034 07-25474 07-27222 07-28474 08-34940  
09-54737  
08-36384 08-37168 08-37252 08-40090 08-40292  
09-58483 
08-48144 08-48160 08-49360 08-49836 09-51664  
07-28724  
09-54942 09-55267 09-56250 09-56291 09-56315 09-57617 09-58071 09-58215 09-58481 09-58495  
07-31221  
09-59654 09-60890 *09-63801  
08-37330  
08-43510  
09-54836  
09-58878 
07-29217  
07-31350  
08-37373  
08-44047  
09-55439  
09-58985 
07-30075  
07-30383  
08-37405  
08-45833  
09-56328  
09-59541 
07-30318  
08-37676  
08-37450  
08-46143  
09-57224  
09-58355 
07-30362  
08-46883  
08-37646  
08-46662  
09-57244  
07-22603 
07-28652  
08-38049  
08-41776  
08-47368  
08-47539  
08-48966 
09-53197  
09-53372  
09-53569  
09-55916  
09-57165  
07-12368 
07-16667  
07-17938  
07-19218  
07-20942  
07-23163  
07-23960 
07-24034  
07-25474  
07-27222  
07-28474  
08-34940  
08-35010 
08-36384  
08-37168  
08-37252  
08-40090  
08-40292  
08-47830 
08-48144  
08-48160  
08-49360  
08-49836  
09-51664  
09-54128 
09-54942  
09-55267  
09-56250  
09-56291  
09-56315  
09-57553 
09-57617  
09-58071  
09-58215  
09-58481  
09-58495  
09-59460 
09-59654  
09-60890  
*09-63801  
*09-63391  
*09-63391  
*09-63416 *09-63532 *09-63546  
*09-63416  
*09-63982 
*09-63532  
*09-63546  
*09-63536  
*09-63536  
*09-63454  
*09-63454  
*09-63479  
*09-63479  
*09-63441 
*09-63916  
*09-63916  
*09-63975  
*09-63975  
Line 1,467: Line 1,073:
*09-63999  
*09-63999  
*09-64004  
*09-64004  
*09-64015 
*09-64040 
*CR written as a result of NRC inspection  
*CR written as a result of NRC inspection  
Audits and Self-assessments  
Audits and Self-assessments  
BV-SA-08-086, "BVPS Inservice  
BV-SA-08-086, "BVPS Inservice Testing (1ST) Program Snapshot Self-Assessment Plan."  
Testing (1ST) Program Snapshot Self-Assessment  
BV-SA-08-007, "CAP Effectiveness."  
Plan." BV-SA-08-007, "CAP Effectiveness." Fleet Self-assessment  
Fleet Self-assessment of Use of Operating Experience at Beaver Valley, Perry and Davis Berry,  
of Use of Operating  
May 2008.  
Experience  
BV-SA-08-009, "Focused Self-Assessment of Beaver Valley Work Management Performance  
at Beaver Valley, Perry and Davis Berry, May 2008. BV-SA-08-009, "Focused Self-Assessment  
Indicators"  
of Beaver Valley Work Management  
BV-SA-08-080  
Performance  
Operating Experience  
Indicators" BV-SA-08-080  
OE 28133  
Operating  
OE 24688  
Experience  
OE 24689  
OE 28133 OE 24688 OE 24689 IN 2008-06 SEN 274, "Multiple  
IN 2008-06  
Reactor Coolant Pump Seal Failures During Cooldown" Attachment   
SEN 274, "Multiple Reactor Coolant Pump Seal Failures During Cooldown"  
Attachment  
 
A-4  
Procedures  
Procedures  
NOP-LP-2001, Corrective  
NOP-LP-2001, Corrective Action Program, Rev. 22  
Action Program, Rev. 22 NOBP-LP-2011, FENOC Cause Analysis, Rev. 9 1/2-EPP-IP-7.1, Emergency  
NOBP-LP-2011, FENOC Cause Analysis, Rev. 9  
Equipment  
1/2-EPP-IP-7.1, Emergency Equipment Inventory and Maintenance Procedure, Rev. 22  
Inventory  
1/2-EPP-IP-7.1, Emergency Equipment Inventory and Maintenance Procedure, Rev. 23  
and Maintenance  
1/2-EPP-IP-7.1.F09, Emergency Inventory Checklist - Primary Assembly Areas, Rev. 4  
Procedure, Rev. 22 1/2-EPP-IP-7.1, Emergency  
1/2-EPP-IP-7.1.F09, Emergency Inventory Checklist - Primary Assembly Areas, Rev. 5  
Equipment  
EPP-PLAN-SECTION-6, Emergency Measures, Rev. 25  
Inventory  
EPP-PLAN-SECTION-7, Emergency Facilities and Equipment, Rev. 25  
and Maintenance  
NOP-LP-5004, Equipment Important to Emergency Response, Rev. 0  
Procedure, Rev. 23 1/2-EPP-IP-7.1.F09, Emergency  
BVRM-EP-5003, Equipment Important to Emergency Response, Rev. 1  
Inventory  
1/2-EPP-IP-7.2, Administration of Emergency Preparedness Plan Drills and Exercises, Rev. 13  
Checklist  
1/2-EPP-IP-3.2, Site Assembly and Personnel Accountability, Rev. 18  
-Primary Assembly Areas, Rev. 4 1/2-EPP-IP-7.1.F09, Emergency  
10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 19  
Inventory  
10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 20  
Checklist  
10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 23  
-Primary Assembly Areas, Rev. 5 EPP-PLAN-SECTION-6, Emergency  
20ST-11.1, Low Head Safety Injection Pump [2SIS*P21A] Test, Rev. 25  
Measures, Rev. 25 EPP-PLAN-SECTION-7, Emergency  
20M-11.2.B, Setpoints, Rev. 4  
Facilities  
2CMP-11SIS-P-21A-B-1M, Low Head Safety Injection Pump Overhaul, Issue 4, Rev. 9  
and Equipment, Rev. 25 NOP-LP-5004, Equipment  
10ST-24.4, Steam Turbine Driven Auxiliary Feed Pump Test [1 FW-P-2], Rev. 42  
Important  
10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 40  
to Emergency  
20ST-24.4, Steam Driven Auxiliary Feed Pump [2FWE*P22] Quarterly Test, Rev. 64  
Response, Rev. 0 BVRM-EP-5003, Equipment  
20ST-24.4A, Steam Driven Auxiliary Feed Pump [2FWE*P22] Full Flow Test, Rev. 20  
Important  
NOBP-LP-1107, Security Operating Experience Guidelines, Rev. 0  
to Emergency  
20M-53A.1.A-0.11, Beaver Valley Power Station Unit 2 Verification of Automatic  
Response, Rev. 1 1/2-EPP-IP-7.2, Administration  
Actions, Rev. 6  
of Emergency  
20M-53A.1.A-0.11, Beaver Valley Power Station Unit 2 Containment Isolation Phase A  
Preparedness  
Checklist, Issue 1 C Rev. 0  
Plan Drills and Exercises, Rev. 13 1/2-EPP-IP-3.2, Site Assembly and Personnel  
NOP-MS-4001, Warehousing, Rev. 6  
Accountability, Rev. 18 10ST-15.1, [1CC-P-1A]  
NOBP-OM-2031, Outage Management Scheduling Process, Rev. 3  
Quarterly  
NOBP-OP-0004, Component Mispositioning, Rev. 2  
Test, Rev. 19 10ST-15.1, [1CC-P-1A]  
NOP-OP-1001, Clearance/Tagging Program, Rev. 11  
Quarterly  
BVBP-OPS-0004, Operations Clearance Coordinator, Rev. 7  
Test, Rev. 20 10ST-15.1, [1CC-P-1A]  
1/2-ADM-2017.F01, Beaver Valley Power Station Vendor Technical Information Review Form-
Quarterly  
Low Head Safety Injection Pump Instruction Manual, Rev. 5  
Test, Rev. 23 20ST-11.1, Low Head Safety Injection  
NOBP-CC-7003, Structured Spare Parts List, Rev. 5  
Pump [2SIS*P21A]  
BVPM-ER-3004, Maintenance Rule (MR) Program Supplemental Guidance, Rev. 0  
Test, Rev. 25 20M-11.2.B, Setpoints, Rev. 4 2CMP-11SIS-P-21A-B-1M, Low Head Safety Injection  
BVBP-OPS-0008, Supplemental Instructions For the Control of Operating Manual Procedures.  
Pump Overhaul, Issue 4, Rev. 9 10ST-24.4, Steam Turbine Driven Auxiliary  
BVPS-OPS-0022, Operating Procedure Development and Revision, Rev. 0  
Feed Pump Test [1 FW-P-2], Rev. 42 10ST-24.9, Turbine-Driven  
NOP-ER-3004, FENOC Maintenance Rule Program, Rev. 1  
AFW Pump [1 FW-P-2] Operability  
SAP Orders/Notifications  
Test, Rev. 40 20ST-24.4, Steam Driven Auxiliary  
Feed Pump [2FWE*P22]  
Quarterly  
Test, Rev. 64 20ST-24.4A , Steam Driven Auxiliary  
Feed Pump [2FWE*P22]  
Full Flow Test, Rev. 20 NOBP-LP-1107, Security Operating  
Experience  
Guidelines, Rev. 0 20M-53A.1.A-0.11 , Beaver Valley Power Station Unit 2 Verification  
of Automatic  
Actions, Rev. 6 20M-53A.1.A-0.11 , Beaver Valley Power Station Unit 2 Containment  
Isolation  
Phase A Checklist, Issue 1 C Rev. 0 NOP-MS-4001, Warehousing, Rev. 6 NOBP-OM-2031, Outage Management  
Scheduling  
Process, Rev. 3 NOBP-OP-0004, Component  
Mispositioning, Rev. 2 NOP-OP-1001, Clearance/Tagging  
Program, Rev. 11 BVBP-OPS-0004, Operations  
Clearance  
Coordinator, Rev. 7 1/2-ADM-2017.F01, Beaver Valley Power Station Vendor Technical  
Information  
Review Form-Low Head Safety Injection  
Pump Instruction  
Manual, Rev. 5 NOBP-CC-7003, Structured  
Spare Parts List, Rev. 5 BVPM-ER-3004, Maintenance  
Rule (MR) Program Supplemental  
Guidance, Rev. 0 BVBP-OPS-0008, Supplemental  
Instructions  
For the Control of Operating  
Manual Procedures.  
BVPS-OPS-0022, Operating  
Procedure  
Development  
and Revision, Rev. 0 NOP-ER-3004, FENOC Maintenance  
Rule Program, Rev. 1 SAP Orders/Notifications  
600556345  
600556345  
600544389  
600544389  
200287486  
200287486  
600519950  
600519950  
200221237  
200221237  
Attachment   
Attachment  
 
A-5  
200309431  
200309431  
200287583  
200287583  
200276981  
200276981  
200042681  
200042681  
200172902  
200172902  
200371419  
200371419  
200310030  
200310030  
200254994  
200254994  
600375319  
600375319  
600422084  
600422084  
600423831  
600423831  
200283954  
200283954  
Non-Cited  
Non-Cited Violations and Findings  
Violations  
NCV 05000334/2008003-01, Inadequate Maintenance Procedure Results in Unexpected Terry
and Findings NCV 05000334/2008003-01, Inadequate  
Turbine Speed Increase  
Maintenance  
NCV 05000334/2007004-02, Inadequate Procedure and Monitoring Program for Turbine Driven  
Procedure  
Auxiliary Feedwater Pump Turbine 1 FW-T-2  
Results in Unexpected  
NCV 05000334/2008002-01, Incorrect Jumper Placement during Testing Renders  
Terry Turbine Speed Increase NCV 05000334/2007004-02, Inadequate  
Quench Spray Chemical Addition Inoperable  
Procedure  
NCV 05000334/2007005-05, Inadequate Inspection led to a subsequent failure of a Fuel Transfer  
and Monitoring  
Up-Ender Cable  
Program for Turbine Driven Auxiliary  
FIN 05000412/2008003-02, Deficient Control of Clearance Posting Interrupts Reactor Coolant  
Feedwater  
Charging Path while Vessel Water Level Drained Below the Flange  
Pump Turbine 1 FW-T-2 NCV 05000334/2008002-01, Incorrect  
Surveillance Tests
Jumper Placement  
20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24, 07/28/08  
during Testing Renders Quench Spray Chemical Addition Inoperable  
20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24, 10/20/08  
NCV 05000334/2007005-05, Inadequate  
20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24, 06/30/09  
Inspection  
10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 36,10/23/07  
led to a subsequent  
10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 40,05/11/09  
failure of a Fuel Transfer Up-Ender Cable FIN 05000412/2008003-02, Deficient  
Vendor Manual  
Control of Clearance  
2502.290-001-001, Low Head Safety Injection Pump Instruction Manual, Rev. S  
Posting Interrupts  
2502.290-001-001, Low Head Safety Injection Pump Instruction Manual, Rev. T  
Reactor Coolant Charging Path while Vessel Water Level Drained Below the Flange Surveillance  
Other  
Tests 20ST-11.1, Low Head Safety Injection  
WO 200287486  
Pump [2SIS-P21A]  
Test, Rev. 24, 07/28/08 20ST-11.1, Low Head Safety Injection  
Pump [2SIS-P21A]  
Test, Rev. 24, 10/20/08 20ST-11.1, Low Head Safety Injection  
Pump [2SIS-P21A]  
Test, Rev. 24, 06/30/09 10ST-24.9, Turbine-Driven  
AFW Pump [1 FW-P-2] Operability  
Test, Rev. 36,10/23/07  
10ST-24.9, Turbine-Driven  
AFW Pump [1 FW-P-2] Operability  
Test, Rev. 40,05/11/09  
Vendor Manual 2502.290-001-001, Low Head Safety Injection  
Pump Instruction  
Manual, Rev. S 2502.290-001-001, Low Head Safety Injection  
Pump Instruction  
Manual, Rev. T Other WO 200287486  
Feedback Form #2008-1448  
Feedback Form #2008-1448  
PM Change Request BV-REV.-08-4731  
PM Change Request BV-REV.-08-4731  
SAP Report -Bill of Materials  
SAP Report - Bill of Materials for Low Head Safety Injection Pump 2SIS-P21A  
for Low Head Safety Injection  
SAP Report - Bill of Materials for Low Head Safety Injection Pump 2SIS-P21B  
Pump 2SIS-P21A  
2SIS-P21A Vibration Trend Data 03/24/1998 - 06/30/2009  
SAP Report -Bill of Materials  
Beaver Valley System Health Report 2008-1  
for Low Head Safety Injection  
Beaver Valley System Health Report 2008-2  
Pump 2SIS-P21B  
Beaver Valley System Health Report 2008-3  
2SIS-P21A  
Beaver Valley System Health Report 2008-4  
Vibration  
Attachment  
Trend Data 03/24/1998  
 
-06/30/2009  
A-6  
Beaver Valley System Health Report 2008-1 Beaver Valley System Health Report 2008-2 Beaver Valley System Health Report 2008-3 Beaver Valley System Health Report 2008-4 Attachment   
Beaver Valley System Health Report 2009-1  
Beaver Valley System Health Report 2009-1 Weekly Operating  
Weekly Operating Experience Summary - August 3, 2009  
Experience  
Maintenance Rule System Basis Document Unit 2 System 47, Rev. 5  
Summary -August 3, 2009 Maintenance  
Maintenance Rule System Basis Document Unit 2 System 47, Rev. 6  
Rule System Basis Document Unit 2 System 47, Rev. 5 Maintenance  
Licensing Requirements Manual, Rev. 52  
Rule System Basis Document Unit 2 System 47, Rev. 6 Licensing  
Protective Tagout 2BVP-CYC-013-1 2R13-07-EDS-00B  
Requirements  
Unit 2 Shift Narrative Logs May 5, 2008 to May 7, 2008  
Manual, Rev. 52 Protective  
Beaver Valley Unit 2 System Health Report 2009-2, "System 43 - Unit 2 Radiation Monitoring  
Tagout 2BVP-CYC-013-1  
System"  
2R13-07-EDS-00B  
Beaver Valley Unit 1 System Health Report 2009-2, "System 43 - Unit 1 Radiation Monitoring  
Unit 2 Shift Narrative  
System"  
Logs May 5, 2008 to May 7, 2008 Beaver Valley Unit 2 System Health Report 2009-2, "System 43 -Unit 2 Radiation  
ADAMS  
Monitoring  
BV  
System" Beaver Valley Unit 1 System Health Report 2009-2, "System 43 -Unit 1 Radiation  
CAP  
Monitoring  
CFR  
System" ADAMS BV CAP CFR CR DRP ECP FENOC IMC IR 1ST MRB NCV NRC OA OE PARS  
CR  
PI&R ROP SCWE SOP TDAFWP WO LIST OF ACRONYMS Agencywide  
DRP  
Documents  
ECP  
Access and Management  
FENOC  
System Beaver Valley Corrective  
IMC  
Action Program Code of Federal Regulations  
IR  
Condition  
1ST  
Report Division of Reactor Projects Employee Concerns Program  
MRB  
FirstEnergy  
NCV  
Nuclear Operating  
NRC  
Company Inspection  
OA  
Manual Chapter Inspection  
OE  
Report Inservice  
PARS  
Test Management  
PI&R  
Review Board Non-Cited  
ROP  
Violation  
SCWE  
Nuclear Regulatory  
SOP  
Commission  
TDAFWP  
WO  
LIST OF ACRONYMS  
Agencywide Documents Access and Management System
Beaver Valley  
Corrective Action Program  
Code of Federal Regulations  
Condition Report
Division of Reactor Projects  
Employee Concerns Program  
FirstEnergy Nuclear Operating Company
Inspection Manual Chapter  
Inspection Report
Inservice Test
Management Review Board  
Non-Cited Violation  
Nuclear Regulatory Commission  
Other Activities  
Other Activities  
Operating  
Operating Experience  
Experience  
Publicly Available Records System  
Publicly Available  
Problem Identification and Resolution  
Records System Problem Identification  
Reactor Oversight Process
and Resolution  
Safety Conscious Work Environment  
Reactor Oversight  
Significance Determination Process
Process Safety Conscious  
Turbine Driven Auxiliary Feedwater Pump
Work Environment  
Work Order  
Significance  
Attachment
Determination  
Process Turbine Driven Auxiliary  
Feedwater  
Pump Work Order Attachment
}}
}}

Latest revision as of 08:52, 14 January 2025

IR 05000334-09-008, IR 05000412-09-008; 08/17/2009 - 09/03/2009; Beaver Valley Power Station, Units 1 & 2; Biennial Baseline Inspection of the Identification and Resolution of Problems
ML092920008
Person / Time
Site: Beaver Valley
Issue date: 10/15/2009
From: Racquel Powell
NRC/RGN-I/DRP/PB7
To: Harden P
FirstEnergy Nuclear Operating Co
powell r j
References
IR-09-008
Download: ML092920008 (22)


See also: IR 05000334/2009008

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

475 ALLENDALE ROAD

KING OF PRUSSIA, PA 19406-1415

October 15, 2009

Mr. Paul Harden

Site Vice President

FirstEnergy Nuclear Operating Company

Beaver Valley Power Station

P. O. Box 4, Route 168

Shippingport, PA 15077

SUBJECT:

BEAVER VALLEY POWER STATION - NRC PROBLEM IDENTIFICATION

AND RESOLUTION INSPECTION REPORT 05000334/2009008 AND

05000412/2009008

Dear Mr. Harden:

On September 3,2009, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Beaver Valley Power Station Units 1 and 2. The enclosed report documents

the inspection results, which were discussed on September 3,2009, with Mr. Roy Brosi and

other members of your staff.

This inspection was an examination of activities conducted under your license as they relate to

the identification and resolution of problems, and compliance with the Commission's rules and

regulations and the conditions of your operating license. Within these areas, the inspection

involved examination of selected procedures and representative records, observations of

activities, and interviews with personnel.

Based on the samples selected for review, the inspection team concluded that FirstEnergy

Nuclear Operating Company (FENOC) was generally effective in identifying, evaluating and

resolving problems. FENOC personnel identified problems at a low threshold and entered them

into the Corrective Action Program (CAP). FENOC personnel screened issues appropriately for

operability and reportability, and prioritized issues commensurate with the safety significance of

the problems. Root and apparent cause analyses appropriately considered extent of condition,

generic issues, and previous occurrences. Corrective actions addressed the identified causes

and were typically implemented in a timely manner. However, the inspectors noted several

examples for improvement in the identification of plant issues, and examples where evaluations

lacked rigor to fully explore the corrective actions needed to address the issue.

This report documents one NRC-identified finding of very low safety significance (Green). The

finding was determined to involve a violation of NRC requirements. However, because of its

very low safety significance and because it has been entered into your CAP, the NRC is

treating this finding as a non-cited violation (NCV), in accordance with Section VI.A.1 of the

NRC's Enforcement Policy. If you deny this NCV, you should provide a response with the basis

for your denial, within 30 days of the date of this inspection report, to the U.S. Nuclear

P. Harden

2

Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-0001, with

copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident

Inspector at the Beaver Valley Power Station. In addition, if you disagree with the

characterization of any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region I, and the NRC Senior Resident Inspector at the Beaver Valley Power

Station. The information you provide will be considered in accordance with Inspection Manual

Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at

~=:'::'~~~~=-'-=:::'!J..!.~~=~~",-= (the Public Electronic Reading Room).

Sincerely,

IRA!

Raymond J. Powell, Chief

Technical Support & Assessment Branch

Division of Reactor Projects

Docket Nos.: 50-334, 50-412

License Nos: DPR-66, NPF-73

Enclosures:

Inspection Report 05000334/2009008; 05000412/2009008

w/Attachment: Supplemental Information

cc w/encls: Distribution via ListServ

P. Harden

3

copies to the Regional Administrator, Region I; the Director, Office of Enforcement, U.S.

Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Senior Resident

Inspector at the Beaver Valley Power Station. In addition, if you disagree with the

characterization of any finding in this report, you should provide a response within 30 days of

the date of this inspection report, with the basis for your disagreement, to the Regional

Administrator, Region I, and the NRC Senior Resident Inspector at the Beaver Valley Power

Station. The information you provide will be considered in accordance with Inspection Manual

Chapter 0305.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of the

NRC's document system (ADAMS). ADAMS is accessible from the NRC Web Site at

http://www.nrc.gov/reading-rm/adams.html(the Public Electronic Reading Room).

Sincerely,

IRAJ

Raymond J. Powell, Chief

Technical Support & Assessment Branch

Division of Reactor Projects

Docket Nos.: 50-334, 50-412

License Nos: DPR-66, NPF-73

Enclosures:

Inspection Report 05000334/2009008; 05000412/2009008

w/Attachment: Supplemental Information

Distribution w/encl: (via e-mail)

S. Collins, RA (R10RAMAILRESOURCE)

M. Dapas, DRA (R10RAMAILRESOURCE)

D. Spindler, DRP, RI

D. Lew, DRP (R1 DRPMAILRESOURCE)

P. Garrett, DRP, OA

J. Clifford, DRP (R1DRPMAIL RESOURCE)

L. Trocine, RI OEDO

R. Bellamy, DRP

RIDSNRRPMBEAVERVAllEY RESOURCE

G. Barber, DRP

ROPreportsResource@nrc.qov

C. Newport, DRP

Region I Docket Room (with concurrences)

J. Greives, DRP

D. Werkheiser, DRP, SRI

SUNSI Review Complete: tcs

(Reviewer's Initials)

ML092920008

DOCUMENT NAME: G:\\DRP\\BRANCH TSAB\\lnspection Reports\\Beaver Valley PI&R 2009\\BV PIR

IR2009008revO.doc

After declaring this document "An Official Agency Record" it will be released to the Public.

To receive acopy of this document, indicate In the box: 'C' =Copy without attachment/enclosure 'E" =Copy with attachment/enclosure "N" =No copy

OFFICE:

RI/DRP

RI/DRP

NAME:

TSetzer/tcs

RBeliamy/rjp for

DATE:

10/13109

10/14/09

Docket Nos.

License Nos.

Report Nos.

Licensee:

Facility:

Location:

Dates:

Team Leader:

Inspectors:

Approved by:

1

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

50-334, 50-412

DPR-66, NPF-73

05000334/2009008 and 05000412/2009008

FirstEnergy Nuclear Operating Company (FENOC)

Beaver Valley Power Station, Units 1 and 2

Post Office Box 4

Shippingport, PA 15077

August 17 through September 3, 2009

Thomas Setzer, PE, Senior Project Engineer

Division of Reactor Projects (DRP)

Jeffery Bream, Project Engineer, DRP

Elizabeth Keighley, Reactor Inspector, DRP

David Spindler, Beaver Valley Resident Inspector, DRP

Raymond J. Powell, Chief

Technical Support &Assessment Branch

Division of Reactor Projects

Enclosure

2

SUMMARY OF FINDINGS

IR 05000334/2009008, IR 05000412/2009008; 08/17/2009 - 09/03/2009; Beaver Valley Power

Station, Units 1 & 2; Biennial Baseline Inspection of the Identification and Resolution of Problems.

One finding was identified in the area of prioritization and evaluation of issues.

This team inspection was performed by three NRC regional inspectors and one resident

inspector. One finding of very low safety significance (Green) was identified during this

inspection and was classified as a non-cited violation (NCV). The significance of most findings is

indicated by their color (Green, White, Yellow, Red) using NRC Inspection Manual Chapter (IMC) 0609, "Significance Determination Process" (SOP). The cross-cutting aspect was determined

using IMC 0305, "Operating Reactor Assessment Program." Findings for which the SOP does

not apply may be Green or be assigned a severity level after NRC management review. The

NRC's program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, "Reactor Oversight Process," Revision 4, December 2006.

Identification and Resolution of Problems

The inspectors concluded that FENOC was, in general, effective in identifying, evaluating, and

resolving problems. Beaver Valley personnel identified problems at a low threshold and entered

them into the Corrective Action Program (CAP). The inspectors determined that Beaver Valley

personnel screened issues appropriately for operability and reportability, and prioritized issues

commensurate with the safety significance of the problems. Root and apparent cause analyses

appropriately considered extent of condition, generic issues, and previous occurrences. The

inspectors determined that corrective actions addressed the identified causes and were typically

implemented in a timely manner. However, the inspectors noted one NCV of very low safety

significance in the area of prioritization and evaluation of issues. This issue was entered into

FENOC's CAP during the inspection.

FENOC's audits and self-assessments reviewed by the inspectors were thorough and probing.

Additionally, the inspectors concluded that FENOC adequately identified, reviewed, and applied

relevant industry operating experience (OE) to the Beaver Valley Power Station. Based on

interviews, observations of plant activities, and reviews of the CAP and the Employees Concerns

Program (ECP), the inspectors did not identify any concerns with site personnel willingness to

raise safety issues, nor did the inspectors identify conditions that could have had a negative

impact on the site's safety conscious work environment (SCWE).

Cornerstone: Mitigating Systems

Green. The inspectors identified an NCV of very low safety significance (Green) of

10 CFR 50.65(a)(2), "Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants," due to FENOC personnel's failure to demonstrate that the

10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches was

effectively controlled through the performance of appropriate preventive maintenance.

Specifically, as evidenced by repeat dual position indications of containment isolation

valves in the control room between 2007 and 2009 resulting in 21 unplanned entries into

Technical Specification 3.6.3, the containment isolation valve system 10 CFR 50.65(a)(2)

performance demonstration was no longer justified in accordance with Maintenance Rule

Enclosure

3

implementing procedure guidance. This should have resulted in placement of the

containment isolation valve system in 10 CFR 50.65(a)(1) for goal setting and monitoring.

FENOC entered this issue into the CAP (CR 09-64040).

The inspectors determined the finding was more than minor because it is associated with

the Equipment Performance attribute of the Mitigating Systems cornerstone and adversely

affected the cornerstone objective of ensuring the reliability of systems that respond to

initiating events to prevent undesirable consequences. The finding was determined to be

of very low safety significance (Green) because the finding did not involve a design or

qualification deficiency resulting in loss of operability or functionality, did not result in a

loss of system safety function, and did not screen as potentially risk significant due to

external initiating events. The inspectors determined that this finding had a cross-cutting

aspect in the "Corrective Action Program" component of the Problem Identification and

Resolution cross-cutting area because FENOC did not take appropriate corrective actions

to address safety issues and adverse trends associated with faulty containment isolation

valve limit switches in a timely manner, commensurate with their safety significance and

complexity P.1(d). (Section 40A2.1c)

Enclosure

.1

4

REPORT DETAILS

4.

OTHER ACTIVITIES (OA)

40A2 Problem Identification and Resolution (PI&R) (71152B)

Assessment of the Corrective Action Program Effectiveness

a.

Inspection Scope

The inspectors reviewed FENOC's procedures that describe the CAP at the Beaver Valley

Power Station. FENOC personnel identified problems by initiating condition reports (CRs)

for conditions adverse to quality, plant equipment deficiencies, industrial or radiological

safety concerns, and other significant issues. Condition reports were subsequently

screened for operability and reportability, and categorized by significance, which included

levels SR (significant condition adverse to quality, root cause), AR (adverse condition, root

cause), AA (adverse condition, full apparent cause), AL (adverse condition, limited

apparent cause), AF (adverse condition, fix), and AC (adverse condition, close). CRs

were assigned to personnel for evaluation and resolution or trending.

The inspectors evaluated the process for assigning and tracking issues to ensure that

issues were screened for operability and reportability, prioritized for evaluation and

resolution in a timely manner commensurate with their safety significance, and tracked to

identify adverse trends and repetitive issues. In addition, the inspectors interviewed plant

staff and management to determine their understanding of, and involvement with, the

CAP.

The inspectors reviewed CRs selected across the seven cornerstones of safety in the

NRC's Reactor Oversight Process (ROP) to determine if site personnel properly identified,

characterized, and entered problems into the CAP for evaluation and resolution. The

inspectors selected items from functional areas that included physical security,

emergency preparedness, engineering, maintenance, operations, and radiation safety to

ensure that FENOC appropriately addressed problems identified in these functional areas.

The inspectors selected a risk-informed sample of CRs that had been issued since the

last NRC Problem Identification and Resolution (PI&R) inspection conducted in April 2007.

Insights from the station's risk analyses were considered to focus the sample selection

and plant walkdowns on risk-significant systems and components. The corrective action

review was expanded to five years for evaluation of identified concerns within CRs relative

to radiation monitors.

The inspectors selected items from various processes at Beaver Valley to verify that they

were appropriately considered for entry into the CAP. Specifically, the inspectors

reviewed a sample of Maintenance Rule functional failure evaluations, operability

determinations, system health reports, work orders (WOs), and issues entered into the

Employee Concerns Program (ECP). The inspectors inspected plant areas including the

turbine buildings, safeguards buildings, intake structure, emergency diesel generator

buildings, yard areas, security areas, and control room.

Enclosure

5

The inspectors reviewed CRs to assess whether FENOC personnel adequately evaluated

and prioritized issues. The CRs reviewed encompassed the full range of evaluations,

including root cause analyses, full apparent cause evaluations, limited apparent cause

analyses, and common cause analyses. A sample of CRs that were assigned lower

levels of significance which did not include formal cause evaluations (AF and AC

significance levels) were also reviewed by the inspectors to ensure they were

appropriately classified. The inspectors' review included the appropriateness of the

assigned significance, the scope and depth of the analysis, and the timeliness of

resolution. The inspectors assessed whether the evaluations identified likely causes for

the issues and identified appropriate corrective actions to address the identified causes.

As part of this review, the inspectors interviewed various station personnel to fully

understand details within the evaluations and the proposed and completed corrective

actions. The inspectors observed management review board (MRB) meetings in which

FENOC personnel reviewed new CRs for prioritization and assignment. Further, the

inspectors reviewed equipment operability determinations and extent-of-condition reviews

for selected CRs to verify these specific reviews adequately addressed equipment

operability and the extent of problems.

The inspectors' review of CRs also focused on the associated corrective actions in order

to determine whether the actions addressed the identified causes of the problems. The

inspectors reviewed CRs for adverse trends and repetitive problems to determine whether

corrective actions were effective in addressing the broader issues. The inspectors

reviewed FENOC's timeliness in implementing. corrective actions and effectiveness in

precluding recurrence for significant conditions adverse to quality. Lastly, the inspectors

reviewed CRs associated with NRC non-cited violations (NCV) and findings since the last

PI&R inspection to determine whether FENOC personnel properly evaluated and resolved

the issues. Specific documents reviewed during the inspection are listed in the

Attachment to this report.

b.

Assessment

Effectiveness of Problem Identification

Based on the selected samples reviewed, plant walkdowns, and interviews of site

personnel, the inspectors determined that, in general, FENOC personnel identified

problems and entered them into the CAP at a low threshold. For the issues reviewed, the

inspectors noted that problems or concerns had been appropriately documented in

enough detail to understand the issues. Approximately 19,000 CRs had been written by

FENOC personnel since January 2007. The inspectors noted that the Security

department had generated significantly less CRs when compared to the rest of the site.

Interviews with Security personnel revealed that they had received adequate training,

displayed a willingness to raise issues, and had ample access to computers; however,

there was a reliance on the shift Captain to enter issues into the CAP.

The inspectors observed managers and supervisors at MRB meetings appropriately

questioning and challenging CRs to ensure clarity of the issues. The inspectors

determined that FENOC personnel trended equipment and programmatic issues, and CR

descriptions appropriately included reference to repeat occurrences of issues. The

Enclosure

6

inspectors concluded that personnel were identifying trends at low levels.

The inspectors toured plant areas including the turbine buildings, safeguards buildings,

intake structure, emergency diesel generator buildings, yard areas, security areas and

control room to determine if FENOC personnel identified plant issues at the proper

threshold. Housekeeping in all areas, with the exception of the Unit 2 intake structure,

was noted to be improved since the 2007 NRC PI&R inspection. During the plant

walkdown, the inspectors identified three examples of adverse conditions that had not

been identified by FENOC. The following issues were entered into the CAP for evaluation

and resolution:

During an inspection of the east end of the main intake structure, the inspectors

identified an oxygen bottle strapped to an Appendix R ladder (a ladder used by

plant personnel for implementing the site fire protection program). Restraining the

oxygen bottle and Appendix R ladder together in this fashion represented a minor

procedure violation of Beaver Valley procedure, 1/2-PIP-G01, "Securing

Transient/Temporary/Stored Equipment in Safety-Related Areas." This issue is

minor because there was no adverse impact to plant safety equipment, and there

was only minimal impact on operator fire response times. FENOC entered this

into the CAP (CR 09-63536).

During an inspection of the 'D' intake structure cubicle, the inspectors identified

rigging scaffolding with a chainfall that had been left draped over a safety related

component. Scaffold contacting plant equipment represented a minor procedure

violation of Beaver Valley procedure, 1/2-ADM-0810, "Scaffold Erection and

Tagging." The component was not damaged nor had any reduced capability as a

result of the contact with the chainfall. This issue is minor because there was no

loss of operability or adverse impact to the safety related component. FENOC

entered this into the CAP (CR 09-63532).

During an inspection of the Unit 2 Safeguards Building, the inspectors identified

four plastic buckets filled with lubricating oil totaling 20 gallons. The unattended oil

in a safety related fire area represented a minor procedure violation of Beaver

Valley procedure, 1/2-ADM-1906, "Control of Transient Combustible and

Flammable Materials." This issue is minor because the increase in combustible

loading in the room as a result of the unattended oil did not violate the plant fire

hazard analysis. FENOC entered this into the CAP (CR 09-63441).

In accordance with NRC Inspection Manual Chapter 0612, "Power Reactor Inspection

Reports," the above issues constitute violations of minor significance that are not subject

to enforcement action in accordance with the NRC's Enforcement Policy.

Effectiveness of Prioritization and Evaluation of Issues

The inspectors determined that, in general, FENOC personnel appropriately prioritized

and evaluated issues commensurate with their safety significance. CRs were screened

for operability and reportability, categorized by significance, and assigned to a department

for evaluation and resolution. The CR screening process considered human performance

issues, radiological safety concerns, repetitiveness and adverse trends. The inspectors

observed managers and supervisors at MRB meetings appropriately questioning and

challenging CRs to ensure appropriate prioritization.

Enclosure

7

CRs were categorized for evaluation and resolution commensurate with the significance of

the issues. Based on the sample of CRs reviewed, the guidance provided by the FENOC

implementing procedures appeared sufficient to ensure consistency in categorization of

the issues. Operability and reportability determinations were performed when conditions

warranted and the evaluations supported the conclusions. Causal analyses appropriately

considered extent of condition, generic issues, and previous occurrences. During this

inspection, the inspectors noted that, in general, FENOC's root cause analyses were

thorough, and corrective and preventive actions addressed the identified causes.

Additionally, the identified causes were well supported. An NCV was identified for

FENOC's failure to demonstrate that the 10 CFR 50.65(a)(2) performance of the

containment isolation valve limit switches was effectively controlled through the

performance of appropriate preventive maintenance. This NCV is discussed in the

findings section of this assessment area. The inspectors identified the following two

examples of issues that were not fully evaluated or prioritized for corrective action:

  • A root cause evaluation (CR 08-39835) associated with a 2.5 inch drain down of

the Unit 2 reactor coolant system during refueling outage 2R13 did not identify all

corrective actions necessary to address all failed barriers. The inspectors noted

that the root cause evaluation had not included corrective actions to address the

communication failure within operations shifts, and the work management

scheduling issues which contributed to a component tagoutlctearance being

inappropriately implemented. The issue is minor because while corrective actions

were not assigned to address all failed barriers, FENOC had discussed

communication expectations with each operating crew and there have not been

any repeat issues. FENOC entered these issues into the CAP (CR 09-63454 and

09-63479).

The inspectors identified three CRs describing component mispositioning events

(CR 09-59541, CR 09-58355, and CR 09-57224) that were prioritized as CR level

OlAF." The failure to prioritize these CRs as a limited apparent cause (CR level

"AL") represented a minor procedure violation of Beaver Valley procedure, NOBP

OP-0004, "Component Mispositioning." The inspectors reviewed NRC Inspection

Manual Chapter 0612, Appendix E, "Minor Examples," and determined this issue

was minor because there was no loss of operability or safety impact. FENOC

entered this issue into the CAP (CR 09-64004 and CR 09-63975).

In accordance with NRC Inspection Manual Chapter 0612, "Power Reactor Inspection

Reports," these issues constitute violations of minor significance that are not subject

to enforcement action in accordance with the NRC's Enforcement Policy.

Effectiveness of Corrective Actions

The inspectors concluded that corrective actions for identified deficiencies were generally

timely and adequately implemented. For significant conditions adverse to quality,

corrective actions were identified to prevent recurrence. The inspectors concluded that

corrective actions to address NCVs and findings since the last PI&R inspection were

timely and effective. The inspectors identified the following example where corrective

actions were not fully effective in addressing an issue:

Enclosure

8

  • The inspectors reviewed corrective actions taken in response to an NCV

documented in NRC report 05000334/05000412 2007004. CR 07-24074 was

written to ensure bearing temperatures would be monitored when performing

surveillance testing on the turbine driven auxiliary feedpumps (TDAFWP). The

inspectors found that the comprehensive surveillance tests for Unit 1 and Unit 2

(Beaver Valley procedures 10ST-24.9 and 20ST-24.4A, respectively) did not have

a precaution stating that this surveillance was not suitable to be used for post

maintenance testing as there is no guidance prescribed to monitor and achieve

steady bearing temperatures. The inspectors determined that the issue was minor

because the preventive maintenance work order had contained the appropriate

guidance. FENOC entered this issue into the CAP (CR 09-64015).

c.

Findings

Introduction: The inspectors identified an NCV of very low safety significance (Green) of

10 CFR 50.65(a)(2), "Requirements for Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants," due to FENOC personnel's failure to demonstrate that the

10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches was

effectively controlled through the performance of appropriate preventive maintenance.

Specifically, as evidenced by repeat dual position indications of containment isolation

valves in the control room resulting in 21 unplanned entries into Technical Specification 3.6.3, the containment isolation valve system 10 CFR 50.65(a)(2) performance

demonstration was no longer justified in accordance with Maintenance Rule implementing

procedure guidance.

Description: The containment isolation valve system is a risk-significant system that is

scoped within the Maintenance Rule because it is a system, structure, or component

(SSC) required to mitigate accidents/transients and is identified in emergency operating

procedures. The primary Maintenance Rule function of the containment isolation valve

system is to provide a containment isolation function during an event to prevent offsite

radiological release. Additionally, limit switches associated with each containment

isolation valve are scoped within the Maintenance Rule because they provide a function to

indicate valve position in the control room for operators to use during emergency

operating procedures.

In February 2009, during stroke-time testing, an air-operated containment isolation valve

displayed dual indication in the control room, causing the stroke times of the valve to be

indeterminate and causing an unplanned entry into Technical Specification 3.6.3.

Additionally, between January 2007 and July 2009, Technical Specification 3.6.3 had 21

unplanned entries as a result of faulty limit switches on similar containment isolation

valves. This resulted in the FENOC established containment isolation valve system

Maintenance Rule condition monitoring criteria being exceeded, which required FENOC to

perform a Maintenance Rule 10 CFR 50.65(a)(1) evaluation. The Maintenance Rule

(a)(1) evaluation was completed in February 2009 and concluded that the containment

isolation valve system should continue to be monitored in accordance with Maintenance

Rule 10 CFR 50.65(a)(2)., This reinforced a similar decision made in 2007 based on a

Maintenance Rule (a)(1) evaluation recommendation to keep the system in (a)(2) despite

Enclosure

9

the condition monitoring criteria being exceeded due to multiple dual indications in the

control room. The basis of the decision was that the dual indication issue was a result of

faulty limit switches, and that this did not affect the valve's safety related function to close

during an event to prevent offsite radiological release. Site personnel determined the

direct cause was the limit switch being out of adjustment due to a problem with the

required torque. Despite the repeat failures, FENOC failed to implement or revise

preventive maintenance practices for these limit switches. Subsequently, the

Maintenance Rule Steering Committee approved a revision to clarify the monitoring

criteria for the containment isolation valve system, which would exclude future indication

problems that did not affect the valve's ability to isolate containment. However, it failed to

take into account the limit switches' Maintenance Rule function in emergency operating

procedures, specifically, the ability to accurately indicate valve position in the control room

during an event. Following the change to the condition monitoring criteria, the site had

seven valves display dual indication in the control room between February 2009 and June

2009 that FENOC concluded did not affect valve operability.

The inspectors concluded that the numerous dual indications of the limit switches should

have been evaluated against FENOC's Maintenance Rule condition monitoring criteria

and should have resulted in placement of the containment isolation valve system in

10 CFR 50.65(a)(1) for goal setting and monitoring. FENOC performed an extent of

condition review on two other valves of the same model, and determined that the torque

on the limit switch fasteners needed to be adjusted. FENOC corrected the torque issue

and has implemented plans to install a button tab on the limit switches to minimize

misalignment causing dual indications.

Analysis: The inspectors determined that the failure to demonstrate that the

10 CFR 50.65{a)(2) performance of the containment isolation valve limit switches was

effectively controlled through the performance of appropriate preventive maintenance was

a performance deficiency within FENOC personnel's ability to foresee and correct and

should have been prevented. Traditional Enforcement did not apply, as the issue did not

have actual or potential safety consequence, had no willful aspects, nor did it impact the

NRC's ability to perform its regulatory function.

A review of NRC Inspection Manual Chapter (IMC) 0612, Appendix E, "Minor Examples,"

revealed that no minor examples were applicable to this finding. The inspectors

determined the finding was more than minor because it is associated with the Equipment

Performance attribute of the Mitigating Systems cornerstone and adversely affected the

cornerstone objective of ensuring the reliability of systems that respond to initiating events

to prevent undesirable consequences. Specifically, the dual indication of containment

isolation valves in the control room due to faulty limit switches presents a challenge to the

operators during event response while implementing emergency operating procedures,

and has resulted in 21 unplanned Technical Specification entries. The numerous dual

indication instances should have caused the containment isolation valve system to be

placed in 10 CFR 50.65(a)(1) for goal setting and monitoring. The inspectors determined

the significance of the finding using IMC 0609.04, "Phase 1

Initial Screening and

Characterization of Findings." The finding was determined to be of very low safety

significance (Green) because the finding did not involve a design or qualification

deficiency resulting in loss of operability or functionality, did not result in a loss of system

Enclosure

10

safety function, and did not screen as potentially risk significant due to external initiating

events.

The inspectors determined that this finding had a cross-cutting aspect in the "Corrective

Action Program" component of the Problem Identification and Resolution cross-cutting

area because FENOC did not take appropriate corrective actions to address safety issues

and adverse trends associated with faulty containment isolation valve limit switches in a

timely manner, commensurate with their safety significance and complexity [P.1 (d)).

Enforcement: 10 CFR 50.65(a)(1) requires, in part, that holders of an operating license

shall monitor the performance or condition of SSCs within the scope of the monitoring

program as defined in 10 CFR 50.65(b) against licensee-established goals, in a manner

sufficient to provide reasonable assurance that such SSCs are capable of fulfilling their

intended functions. 10 CFR 50.65(a)(2) states, in part, that monitoring as specified in

10 CFR 50.65(a)(1) is not required where it has been demonstrated that the performance

or condition of an SSC is being effectively controlled through the performance of

appropriate preventative maintenance, such that the SSC remains capable of performing

its intended function.

Contrary to the above, between 2007 and 2009, FENOC personnel failed to demonstrate

that the 10 CFR 50.65(a)(2) performance of the containment isolation valve limit switches

was effectively controlled through the performance of appropriate preventive

maintenance. FENOC has performed an extent of condition review and has initiated

corrective actions to install a button tab on the limit switches to minimize misalignment

causing the dual indications. Because this violation was of very low safety significance

and has been entered into the CAP (CR 09-64040), this violation is being treated as an

NCV, consistent with the NRC Enforcement Policy (NCV 05000314,412/2009008-01:

Containment Isolation Valve System 10 CFR 50.65 (a)(2) Performance

Demonstration Not Met) .

. 2

Assessment of the Use of Operating Experience

a.

Inspection Scope

The inspectors selected a sample of CRs associated with the review of industry Operating

Experience (OE) to determine whether FENOC personnel appropriately evaluated the OE

information for applicability to Beaver Valley and had taken appropriate actions, when

warranted. The inspectors reviewed CR evaluations of OE documents associated with a

sample of NRC Generic Letters and Information Notices to ensure that FENOC

adequately considered the underlying problems associated with the issues for resolution

via their CAP. The inspectors also observed plant activities to determine if industry OE

was considered during the performance of routine activities. Specific documents

reviewed during the inspection are listed in the Attachment to this report.

b.

Assessment

The inspectors determined that, in general, FENOC appropriately considered industry OE

information for applicability, and used the information for corrective and preventive actions

Enclosure

11

to identify and prevent similar issues when appropriate. The inspectors determined that

OE was appropriately applied and lessons learned were communicated and incorporated

into plant operations. The inspectors observed that industry OE was routinely discussed

and considered during the performance of plant activities.

The inspectors reviewed a fleet-level focused self-assessment of OE performed in May

2008. The self-assessment identified a number of weaknesses, specifically:

  • OE was not discussed in system health reports;
  • Roles and responsibilities of Section OE Coordinators were not clearly defined;

Familiarization with SAP, the database used to manage OE, was low at the

Management and Section OE Coordinator levels; and

  • Procedures describing the requirements to process OE were in need of revision to

add clarity.

Although the inspectors noted that corrective actions were not completed until June 2009,

since that time Beaver Valley has made progress in addressing OE program needs. This

has included clearly defining the roles and responsibilities of Section OE Coordinators.

Procedures have been revised and a familiarization guide has been completed with

guidance on how to use SAP efficiently. Training has been completed for Section OE

Coordinators and the backlog of unreviewed OE items has decreased (currently at 2

unreviewed items as compared to over 12 items previously). Finally, a higher level of

accountability has been placed on each department to report backlogged OE items at

weekly plant meetings. With respect to incorporating OE in system health reports, the

inspectors identified that OE continued not to be incorporated in the 2008 and 2009

reports. FENOC entered this issue into the CAP (CR 09-63999).

c.

Findings

No findings of significance were identified .

. 3

Assessment of Self-Assessments and Audits

a.

Inspection Scope

The inspectors reviewed a sample of snapshot self-assessments, focused self

assessments, fleet-level assessments, and a variety of self-assessments focused on

various plant programs. These reviews were performed to determine if problems

identified through these assessments were entered into the CAP, and whether corrective

actions were initiated to address identified deficiencies. The effectiveness of the

assessments was evaluated by comparing audit and assessment results against

self-revealing and NRC-identified observations made during the inspection. A list of

documents reviewed is included in the Attachment to this report.

b.

Assessment

The inspectors concluded that QA audits and self-assessments were critical, thorough,

and effective in identifying issues. The inspectors observed that these audits and self-

Enclosure

.4

12

assessments were completed by personnel knowledgeable in the subject areas and were

completed to a sufficient depth to identify issues that were then entered into the CAP for

evaluation. Corrective actions associated with the issues were implemented

commensurate with their safety significance. FENOC managers evaluated the results and

initiated appropriate actions to focus on areas identified for improvement.

c.

Findings

No findings of significance were identified .

Assessment of Safety Conscious Work Environment

a.

Inspection Scope

The inspectors performed interviews with station personnel to assess the safety conscious

work environment (SCWE) at Beaver Valley. Specifically, the inspectors interviewed

personnel to determine whether they were hesitant to raise safety concerns to their

management and/or the NRC. The inspectors also interviewed the station Employee

Concerns Program (ECP) coordinator to determine what actions were implemented to

ensure employees were aware of the program and its availability with regard to raising

concerns. The inspectors reviewed the ECP files to ensure that issues were entered into

the CAP when appropriate. The inspectors reviewed site SCWE surveys from 2007 and

2008 to assess any adverse trends in department and site safety culture. A list of

documents reviewed is included in the Attachment to this report.

b.

Assessment

During interviews, plant staff expressed a willingness to use the CAP to identify plant

issues and deficiencies, and stated that they were willing to raise safety issues. All

persons interviewed demonstrated an adequate knowledge of the CAP and ECP. Based

on these limited interviews, the inspectors concluded that there was no evidence of

SCWE concerns and no significant challenges to the free flow of information.

SCWE surveys in 2007 and 2008 showed that the overall SCWE health at Beaver Valley

remained positive. The surveys indicated the staff understands and accepts expectations

and responsibilities for identifying concerns. The surveys indicated FENOC personnel

feel free to approach management with issues and management expectations on safety

and quality are clearly communicated. The surveys indicated lower than average scores

for Radiation Protection, Chemistry, Security, and Site Projects departments. CRs were

generated to help promote improvement in the safety culture of these departments, and

corrective actions were implemented. The inspectors noted that when compared to the

2007 survey, the Operations department had an increase in negative responses in the

2008 survey. This trend had not been entered into the CAP for evaluation since the

negative score averages did not exceed a ten percent cutoff "trigger" for CR generation.

The inspectors questioned this cutoff in that it appeared to potentially limit FENOC's ability

to fully explore year-to-year trends in departments that may not exceed ten percent

negative responses, but decline significantly from the previous survey_ FENOC entered

this issue into the CAP (CR 09-63998).

Enclosure

13

As a result of the survey review, the inspectors completed additional SCWE interviews

with operators to determine if there was a reluctance to raise safety issues. No individuals

expressed any fear to raise issues.

c.

Findings

No findings of significance were identified.

40A6 Meetings, Including Exit

On September 3, 2009, the inspectors presented the inspection results to Mr. Roy Brosi,

Director of Site Performance Improvement, and other members of the Beaver Valley staff.

The inspectors verified that no proprietary information was documented in the report.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

A-1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

Harold Szklinski, Staff Nuclear Specialist

Fulton Schaffner, Staff Nuclear Specialist

Daniel Butor, Staff Nuclear Specialist

Robert Lubert, Supervisor, Nuclear Electrical System Engineering

Francy Mantine, Staff Nuclear Engineer

David Jones, Staff Nuclear Engineer

Philip Slifkin, Staff Nuclear Engineer

Giuseppe Cerasi, Senior Nuclear Specialist

Brian Goff, Supervisor, Nuclear Work Planning

Michael Kienzle, Nuclear Engineering

Pat Pauvlinch, Supervisor, Nuclear Plant System Engineering

Robert Williams, Staff Nuclear Engineer

Joann West, Staff Nuclear Engineer

John Kaminskas, Nuclear Engineer

David Hauser, Superintendent Shift Operations, Unit 2

Christopher Makowka, Root Cause Evaluator

Michael Mitchell, Superintendent Nuclear Work Planning

John Bowden, Superintendent Nuclear Operations Services

Jim Mauck, Senior Nuclear Specialist

Brian Sepelak, Supervisor, Nuclear Compliance

Karl Wolfson, Supervisor, Nuclear Performance Improvement

Colin Keller, Manager, Site Regulatory Compliance

Rich Dibler, Security Support Supervisor

Sue Vincinie, Performance Improvement Senior Consultant

Darrel Batina, Employee Concerns Program Representative

Dutch Chancey, Manager, Employee Concerns (Fleet)

Wayne Mcintire, Beaver Valley Site Safety Specialist

Gary Shildt, Supervisor, Nuclear Projects Engineering

Jack Patterson, Staff Nuclear Engineer

Thomas King, Plant Engineer

Robert Lubert, Plant Engineering Supervisor

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000334, 412/2009008-01

Containment Isolation Valve System 10 CFR 50.65

(a)(2) Performance Demonstration Not Met.

Attachment

A-2

LIST OF DOCUMENTS REVIEWED

Condition ReQorts

08-38146

09-60763

09-55789

08-50881

08-47439

08-46291

08-45288

08-42054

08-36772

07-26862

08-32856

07-14885

07-14208

09-62156

09-62106

09-61128

09-60432

09-59875

09-56773

09-54230

09-52736

08-39941

08-48160

09-57390

09-52275

08-49681

08-33109

07-28371

07-15761

09-61333

08-42790

09-62268

09-59641

09-58307

09-57580

09-57463

09-55267

09-52029

08-48296

09-57822

09-61026

09-60359

09-56525

09-61753

09-57743

08-51000

07-23937

09-59057

09-53803

08-41802

08-32965

03-01371

09-61679

09-62681

09-57726

08-39835

07-18191

07-21962

08-48581

08-50283

09-52719

09-61026

09-63451

09-61453

08-48268

08-44941

08-44947

08-37921

08-44960

07-24074

07-30275

09-63317

08-48482

09-52857

09-63269

09-57857

09-56402

08-34526

08-33776

09-55350

09-52043

07-28809

07-12360

07-14181

07-14185

07-14530

07-14761

07-14934

09-61430

09-61631

09-61878

09-62202

09-62810

07-15636

07-17006

07-17236

07-20147

07-20158

07-22189

07-24552

07-25283

07-28203

07-22004

07-29608

07-30073

09-57198

09-57688

09-57815

09-58598

09-60492

09-60672

09-59088

09-60547

09-61017

07-31483

07-28809

07-12120

08-35376

08-49694

08-43202

08-43205

09-62787

08-48664

08-49518

09-53081

09-53243

09-53762

09-54051

09-55146

09-55719

09-56851

09-56874

09-57268

09-57784

09-58142

07-26688

09-54051

08-48664

07-25046

07-30273

08-38146

07-13076

08-48581

09-60218

04-09895

07-30390

07-32095

08-40472

08-48688

09-60450

06-11217

07-30430

08-32447

08-40490

08-49073

09-60763

07-13021

07-30431

08-32887

08-40519

08-49368

09-61744

07-15001

07-30447

08-33126

08-40575

08-49750

09-62348

07-15444

07-30484

08-33306

08-40579

08-49983

09-62705

07-18894

07-30575

08-33398

08-40587

08-50137

08-37743

07-20907

07-30677

08-33725

08-40753

08-50151

08-37925

07-22891

07-30823

08-35048

08-40867

08-51024

08-38276

07-23543

07-30847

08-35517

08-40932

08-51136

08-38687

07-23933

07-30911

08-35674

08-40970

08-51385

08-38750

07-26020

07-30912

08-36383

08-41330

09-52096

08-39233

Attachment

A-3

07-26065

07-30988

08-36471

08-41450

09-52351

08-39304

07-26326

07-30999

08-36539

08-41691

09-53214

08-39946

07-27423

07-31040

08-37026

08-41723

09-53275

08-46995

07-27469

07-31083

08-37250

08-41801

09-53803

08-47282

07-28007

07-31107

08-37304

08-42046

09-53938

08-47455

07-28012

07-31110

08-37318

08-42627

09-54227

08-47767

07-28471

07-31112

08-37320

08-42847

09-54737

09-58483

07-28724

07-31221

08-37330

08-43510

09-54836

09-58878

07-29217

07-31350

08-37373

08-44047

09-55439

09-58985

07-30075

07-30383

08-37405

08-45833

09-56328

09-59541

07-30318

08-37676

08-37450

08-46143

09-57224

09-58355

07-30362

08-46883

08-37646

08-46662

09-57244

07-22603

07-28652

08-38049

08-41776

08-47368

08-47539

08-48966

09-53197

09-53372

09-53569

09-55916

09-57165

07-12368

07-16667

07-17938

07-19218

07-20942

07-23163

07-23960

07-24034

07-25474

07-27222

07-28474

08-34940

08-35010

08-36384

08-37168

08-37252

08-40090

08-40292

08-47830

08-48144

08-48160

08-49360

08-49836

09-51664

09-54128

09-54942

09-55267

09-56250

09-56291

09-56315

09-57553

09-57617

09-58071

09-58215

09-58481

09-58495

09-59460

09-59654

09-60890

  • 09-63801
  • 09-63391
  • 09-63416
  • 09-63982
  • 09-63532
  • 09-63546
  • 09-63536
  • 09-63454
  • 09-63479
  • 09-63441
  • 09-63916
  • 09-63975
  • 09-63998
  • 09-63999
  • 09-64004
  • 09-64015
  • 09-64040
  • CR written as a result of NRC inspection

Audits and Self-assessments

BV-SA-08-086, "BVPS Inservice Testing (1ST) Program Snapshot Self-Assessment Plan."

BV-SA-08-007, "CAP Effectiveness."

Fleet Self-assessment of Use of Operating Experience at Beaver Valley, Perry and Davis Berry,

May 2008.

BV-SA-08-009, "Focused Self-Assessment of Beaver Valley Work Management Performance

Indicators"

BV-SA-08-080

Operating Experience

OE 28133

OE 24688

OE 24689

IN 2008-06

SEN 274, "Multiple Reactor Coolant Pump Seal Failures During Cooldown"

Attachment

A-4

Procedures

NOP-LP-2001, Corrective Action Program, Rev. 22

NOBP-LP-2011, FENOC Cause Analysis, Rev. 9

1/2-EPP-IP-7.1, Emergency Equipment Inventory and Maintenance Procedure, Rev. 22

1/2-EPP-IP-7.1, Emergency Equipment Inventory and Maintenance Procedure, Rev. 23

1/2-EPP-IP-7.1.F09, Emergency Inventory Checklist - Primary Assembly Areas, Rev. 4

1/2-EPP-IP-7.1.F09, Emergency Inventory Checklist - Primary Assembly Areas, Rev. 5

EPP-PLAN-SECTION-6, Emergency Measures, Rev. 25

EPP-PLAN-SECTION-7, Emergency Facilities and Equipment, Rev. 25

NOP-LP-5004, Equipment Important to Emergency Response, Rev. 0

BVRM-EP-5003, Equipment Important to Emergency Response, Rev. 1

1/2-EPP-IP-7.2, Administration of Emergency Preparedness Plan Drills and Exercises, Rev. 13

1/2-EPP-IP-3.2, Site Assembly and Personnel Accountability, Rev. 18

10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 19

10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 20

10ST-15.1, [1CC-P-1A] Quarterly Test, Rev. 23

20ST-11.1, Low Head Safety Injection Pump [2SIS*P21A] Test, Rev. 25

20M-11.2.B, Setpoints, Rev. 4

2CMP-11SIS-P-21A-B-1M, Low Head Safety Injection Pump Overhaul, Issue 4, Rev. 9

10ST-24.4, Steam Turbine Driven Auxiliary Feed Pump Test [1 FW-P-2], Rev. 42

10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 40

20ST-24.4, Steam Driven Auxiliary Feed Pump [2FWE*P22] Quarterly Test, Rev. 64

20ST-24.4A, Steam Driven Auxiliary Feed Pump [2FWE*P22] Full Flow Test, Rev. 20

NOBP-LP-1107, Security Operating Experience Guidelines, Rev. 0

20M-53A.1.A-0.11, Beaver Valley Power Station Unit 2 Verification of Automatic

Actions, Rev. 6

20M-53A.1.A-0.11, Beaver Valley Power Station Unit 2 Containment Isolation Phase A

Checklist, Issue 1 C Rev. 0

NOP-MS-4001, Warehousing, Rev. 6

NOBP-OM-2031, Outage Management Scheduling Process, Rev. 3

NOBP-OP-0004, Component Mispositioning, Rev. 2

NOP-OP-1001, Clearance/Tagging Program, Rev. 11

BVBP-OPS-0004, Operations Clearance Coordinator, Rev. 7

1/2-ADM-2017.F01, Beaver Valley Power Station Vendor Technical Information Review Form-

Low Head Safety Injection Pump Instruction Manual, Rev. 5

NOBP-CC-7003, Structured Spare Parts List, Rev. 5

BVPM-ER-3004, Maintenance Rule (MR) Program Supplemental Guidance, Rev. 0

BVBP-OPS-0008, Supplemental Instructions For the Control of Operating Manual Procedures.

BVPS-OPS-0022, Operating Procedure Development and Revision, Rev. 0

NOP-ER-3004, FENOC Maintenance Rule Program, Rev. 1

SAP Orders/Notifications

600556345

600544389

200287486

600519950

200221237

Attachment

A-5

200309431

200287583

200276981

200042681

200172902

200371419

200310030

200254994

600375319

600422084

600423831

200283954

Non-Cited Violations and Findings

NCV 05000334/2008003-01, Inadequate Maintenance Procedure Results in Unexpected Terry

Turbine Speed Increase

NCV 05000334/2007004-02, Inadequate Procedure and Monitoring Program for Turbine Driven

Auxiliary Feedwater Pump Turbine 1 FW-T-2

NCV 05000334/2008002-01, Incorrect Jumper Placement during Testing Renders

Quench Spray Chemical Addition Inoperable

NCV 05000334/2007005-05, Inadequate Inspection led to a subsequent failure of a Fuel Transfer

Up-Ender Cable

FIN 05000412/2008003-02, Deficient Control of Clearance Posting Interrupts Reactor Coolant

Charging Path while Vessel Water Level Drained Below the Flange

Surveillance Tests

20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24, 07/28/08

20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24, 10/20/08

20ST-11.1, Low Head Safety Injection Pump [2SIS-P21A] Test, Rev. 24, 06/30/09

10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 36,10/23/07

10ST-24.9, Turbine-Driven AFW Pump [1 FW-P-2] Operability Test, Rev. 40,05/11/09

Vendor Manual

2502.290-001-001, Low Head Safety Injection Pump Instruction Manual, Rev. S

2502.290-001-001, Low Head Safety Injection Pump Instruction Manual, Rev. T

Other

WO 200287486

Feedback Form #2008-1448

PM Change Request BV-REV.-08-4731

SAP Report - Bill of Materials for Low Head Safety Injection Pump 2SIS-P21A

SAP Report - Bill of Materials for Low Head Safety Injection Pump 2SIS-P21B

2SIS-P21A Vibration Trend Data 03/24/1998 - 06/30/2009

Beaver Valley System Health Report 2008-1

Beaver Valley System Health Report 2008-2

Beaver Valley System Health Report 2008-3

Beaver Valley System Health Report 2008-4

Attachment

A-6

Beaver Valley System Health Report 2009-1

Weekly Operating Experience Summary - August 3, 2009

Maintenance Rule System Basis Document Unit 2 System 47, Rev. 5

Maintenance Rule System Basis Document Unit 2 System 47, Rev. 6

Licensing Requirements Manual, Rev. 52

Protective Tagout 2BVP-CYC-013-1 2R13-07-EDS-00B

Unit 2 Shift Narrative Logs May 5, 2008 to May 7, 2008

Beaver Valley Unit 2 System Health Report 2009-2, "System 43 - Unit 2 Radiation Monitoring

System"

Beaver Valley Unit 1 System Health Report 2009-2, "System 43 - Unit 1 Radiation Monitoring

System"

ADAMS

BV

CAP

CFR

CR

DRP

ECP

FENOC

IMC

IR

1ST

MRB

NCV

NRC

OA

OE

PARS

PI&R

ROP

SCWE

SOP

TDAFWP

WO

LIST OF ACRONYMS

Agencywide Documents Access and Management System

Beaver Valley

Corrective Action Program

Code of Federal Regulations

Condition Report

Division of Reactor Projects

Employee Concerns Program

FirstEnergy Nuclear Operating Company

Inspection Manual Chapter

Inspection Report

Inservice Test

Management Review Board

Non-Cited Violation

Nuclear Regulatory Commission

Other Activities

Operating Experience

Publicly Available Records System

Problem Identification and Resolution

Reactor Oversight Process

Safety Conscious Work Environment

Significance Determination Process

Turbine Driven Auxiliary Feedwater Pump

Work Order

Attachment