IR 05000250/2010003: Difference between revisions
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==SUBJECT:== | ==SUBJECT:== | ||
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The report documents one NRC identified and one self-revealing finding of very low safety significance (Green). These findings were determined to involve violations of NRC requirements. However, because of very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Turkey Point. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at Turkey Point. | The report documents one NRC identified and one self-revealing finding of very low safety significance (Green). These findings were determined to involve violations of NRC requirements. However, because of very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Turkey Point. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at Turkey Point. | ||
FPL | FPL | ||
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | |||
Sincerely, | Sincerely, | ||
/RA/ | /RA/ | ||
Daniel W. Rich, Chief Rector Projects Branch 3 Division of Reactor Projects Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41 | |||
Daniel W. Rich, Chief | |||
Rector Projects Branch 3 | |||
Division of Reactor Projects | |||
Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41 | |||
===Enclosure:=== | ===Enclosure:=== | ||
Inspection Report 05000250/2010003 and 05000251/2010003 w/Attachment: Supplemental Information | Inspection Report 05000250/2010003 and 05000251/2010003 | ||
w/Attachment: Supplemental Information | |||
__ML102100318________________ | |||
X SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRS RII:DRS RII:DRP RII:DRS RII:DRS SIGNATURE SON JSS1 by email AND by email GBK1 by email JBH4 by email JAE1 by email AXA1 by email NAME SNinh JStewart ANielsen GKuzo JHamman JEargle AAlen DATE 0728/2010 07/27/2010 07/21/2010 07/21/2010 07/26/2010 07/23/2010 07/27/2010 E-MAIL COPY? | |||
YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:DRP | |||
SIGNATURE MCB by email | |||
NAME MBarillas | |||
DATE 07/26/2010 | |||
E-MAIL COPY? | |||
YES NO YES NO YES NO YES NO YES NO YES NO YES NO | |||
FPL | FPL | ||
REGION II== | REGION II== | ||
Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41 Report No: 05000250/2010003, 05000251/2010003 Licensee: Florida Power & Light Company (FP&L) | Docket Nos.: | ||
Facility: Turkey Point Nuclear Plant, Units 3 & 4 Location: 9760 S. W. 344th Street Homestead, FL 33035 Dates: April 1 to June 30, 2010 Inspectors: J. Stewart, Senior Resident Inspector M. Barillas, Resident Inspector A. Nielsen, Health Physicist (2RS8) | 50-250, 50-251 | ||
G. Kuzo, Senior Health Physicist (2RS8) | |||
J. Hamman, Reactor Inspector (1R17) | License Nos.: | ||
DPR-31, DPR-41 | |||
Report No: | |||
05000250/2010003, 05000251/2010003 | |||
Licensee: | |||
Florida Power & Light Company (FP&L) | |||
Facility: | |||
Turkey Point Nuclear Plant, Units 3 & 4 | |||
Location: | |||
9760 S. W. 344th Street Homestead, FL 33035 | |||
Dates: | |||
April 1 to June 30, 2010 | |||
Inspectors: | |||
J. Stewart, Senior Resident Inspector | |||
M. Barillas, Resident Inspector A. Nielsen, Health Physicist (2RS8) | |||
G. Kuzo, Senior Health Physicist (2RS8) | |||
J. Hamman, Reactor Inspector (1R17) | |||
S. Ninh, Senior Project Engineer (1R17) | S. Ninh, Senior Project Engineer (1R17) | ||
J. Eargle, Reactor Inspector (1R17) | J. Eargle, Reactor Inspector (1R17) | ||
A. Alen, Reactor Inspector (1R17) | A. Alen, Reactor Inspector (1R17) | ||
Approved by: D. Rich, Branch, Chief Reactor Projects Branch 3 Division of Reactor Projects Enclosure | |||
Approved by: | |||
D. Rich, Branch, Chief Reactor Projects Branch 3 Division of Reactor Projects | |||
Enclosure | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
IR 05000250/2010-003, 05000251/2010-003; 4/1/2010 - 6/30/2010; Turkey Point Nuclear | IR 05000250/2010-003, 05000251/2010-003; 4/1/2010 - 6/30/2010; Turkey Point Nuclear | ||
Power Plant, Units 3 and 4; Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation, Followup of Events | |||
The report covered a three month period of inspection by resident inspectors and region based health physicists. Two Green NCVs were identified. The significance of most findings is identified by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP); the cross-cutting aspect was determined using IMC 305, | |||
Operating Reactor Assessment Program; and that findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December, 2006. | Operating Reactor Assessment Program; and that findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December, 2006. | ||
===NRC-Identified=== | ===NRC-Identified=== | ||
& Self-Revealing Findings | & Self-Revealing Findings | ||
===Cornerstone: Initiating Events=== | ===Cornerstone: Initiating Events=== | ||
* | |||
: '''Green.''' | : '''Green.''' | ||
A Self-Revealing Non-cited Violation of Technical Specification 3.1.3.1.b requirements was identified on Unit 3 when position indication for two rod control cluster assemblies (RCCs) drifted out of tolerance with the associated rod group position indication. | A Self-Revealing Non-cited Violation of Technical Specification 3.1.3.1.b requirements was identified on Unit 3 when position indication for two rod control cluster assemblies (RCCs) drifted out of tolerance with the associated rod group position indication. | ||
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* Green The inspectors identified a Green non-cited violation (NCV) of 10 CFR Part 20.1501(a) for the failure to perform adequate surveys to meet the requirements of 10 CFR Part 20 Appendix G. 10 CFR Part 20 Appendix G states that shippers of radioactive waste must identify and quantify radionuclides contained in each waste container. Specifically, the inspectors determined that the use of resin samples to characterize three shipments of mechanical filters in calendar years 2008 and 2009 was inadequate to ensure proper identification and quantification of the radionuclides present in each container. The licensee entered the issue into their corrective action program as condition report (CR) number 2009-32955. | * Green The inspectors identified a Green non-cited violation (NCV) of 10 CFR Part 20.1501(a) for the failure to perform adequate surveys to meet the requirements of 10 CFR Part 20 Appendix G. 10 CFR Part 20 Appendix G states that shippers of radioactive waste must identify and quantify radionuclides contained in each waste container. Specifically, the inspectors determined that the use of resin samples to characterize three shipments of mechanical filters in calendar years 2008 and 2009 was inadequate to ensure proper identification and quantification of the radionuclides present in each container. The licensee entered the issue into their corrective action program as condition report (CR) number 2009-32955. | ||
The finding is more than minor because it is associated with the Public Radiation Safety cornerstone attribute of Programs and Processes and adversely affects the cornerstone objective of ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. The finding was assessed using the Public Radiation Safety Significance Determination Process (SDP). Based on the fact that subsequent follow up analyses demonstrated that none of the filter waste was under-classified, the finding was determined to be of very low safety significance (Green). This finding has a crosscutting aspect of Human Performance, Decision Making [H.1(b)], because the decision to use resin samples to characterize filter shipments was based on incorrect assumptions, i.e., that spent resin samples would be representative of the filter waste stream, and those assumptions were not demonstrated to be conservative prior to implementation. (Section 2RS8) | The finding is more than minor because it is associated with the Public Radiation Safety cornerstone attribute of Programs and Processes and adversely affects the cornerstone objective of ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. The finding was assessed using the Public Radiation Safety Significance Determination Process (SDP). Based on the fact that subsequent follow up analyses demonstrated that none of the filter waste was under-classified, the finding was determined to be of very low safety significance (Green). This finding has a crosscutting aspect of Human Performance, Decision Making [H.1(b)], because the decision to use resin samples to characterize filter shipments was based on incorrect assumptions, i.e., that spent resin samples would be representative of the filter waste stream, and those assumptions were not demonstrated to be conservative prior to implementation. (Section 2RS8) | ||
===Licensee Identified Violations=== | ===Licensee Identified Violations=== | ||
None | None | ||
=REPORT DETAILS= | =REPORT DETAILS= | ||
Summary of Plant Status: | Summary of Plant Status: | ||
Unit 3: Unit 3 started the period at full power. Reactor power was reduced to 90 percent on June 23 to repair a secondary system pump then returned to full power on June 24 and was at full power for the rest of the inspection period. | Unit 3: Unit 3 started the period at full power. Reactor power was reduced to 90 percent on June 23 to repair a secondary system pump then returned to full power on June 24 and was at full power for the rest of the inspection period. | ||
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==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity (Reactor-R) | Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity (Reactor-R) | ||
{{a|1R01}} | {{a|1R01}} | ||
==1R01 Adverse Weather Protection (02.01 Summer Readiness of Offsite and Alternate AC== | ==1R01 Adverse Weather Protection (02.01 Summer Readiness of Offsite and Alternate AC== | ||
Power Systems, 02.02 Readiness for Extreme Weather Conditions, and 02.04 Readiness to Cope with External Flooding) | |||
Power Systems, 02.02 Readiness for Extreme Weather Conditions, and 02.04 | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R01}} | No findings were identified. {{a|1R01}} | ||
Weather Conditions) | ==1R01 Adverse Weather Protection (02.03, Evaluate Readiness for Impending Adverse Weather Conditions) | ||
== | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors evaluated the implementation of off-normal procedure 0-ONOP-011.1, Intake Canal High Temperature when the intake cooling water exceeded 96 degrees F which coincided with high containment ambient temperatures during the week of June 14. The inspectors verified that Technical Specification 3.6.1.5 high temperature equivalent hours were recorded and tracked. | The inspectors evaluated the implementation of off-normal procedure 0-ONOP-011.1, Intake Canal High Temperature when the intake cooling water exceeded 96 degrees F which coincided with high containment ambient temperatures during the week of June 14. The inspectors verified that Technical Specification 3.6.1.5 high temperature equivalent hours were recorded and tracked. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R04}} | No findings were identified. {{a|1R04}} | ||
==1R04 Equipment Alignment | |||
== | |||
===.1 Partial Equipment Walkdowns=== | ===.1 Partial Equipment Walkdowns=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors conducted three partial alignment verifications of the safety-related systems listed below. These inspections included reviews using operating procedures and piping and instrumentation drawings, which were compared with observed equipment configurations to verify that the critical portions of the systems were correctly aligned to support operability. The inspectors also verified that the licensee had identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems. The inspectors routinely verified that alignment issues were documented in the corrective action program. | The inspectors conducted three partial alignment verifications of the safety-related systems listed below. These inspections included reviews using operating procedures and piping and instrumentation drawings, which were compared with observed equipment configurations to verify that the critical portions of the systems were correctly aligned to support operability. The inspectors also verified that the licensee had identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems. The inspectors routinely verified that alignment issues were documented in the corrective action program. | ||
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===.2 Complete System Walkdown=== | ===.2 Complete System Walkdown=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors performed a detailed review of the alignment and condition of system 062, Unit 4 safety injection, to verify that the existing alignment was consistent with the design. To determine the correct system alignment, the inspectors reviewed Turkey Point Technical Specifications (TS); licensee procedure 4-OSP-202.1, Safety Injection Flowpath Verification; procedure 4-NOP-062, Unit 4 Safety Injection; piping and instrumentation drawing 5614-M-3062; the design basis document; and the FSAR. The inspectors walked down supports and restraints associated with selected piping of the safety injection pumps. During the walkdown, the inspectors reviewed the following: | The inspectors performed a detailed review of the alignment and condition of system 062, Unit 4 safety injection, to verify that the existing alignment was consistent with the design. To determine the correct system alignment, the inspectors reviewed Turkey Point Technical Specifications (TS); licensee procedure 4-OSP-202.1, Safety Injection Flowpath Verification; procedure 4-NOP-062, Unit 4 Safety Injection; piping and instrumentation drawing 5614-M-3062; the design basis document; and the FSAR. The inspectors walked down supports and restraints associated with selected piping of the safety injection pumps. During the walkdown, the inspectors reviewed the following: | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R05}} | No findings were identified. {{a|1R05}} | ||
==1R05 Fire Protection | |||
==1R05 Fire Protection | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
===.1 Fire Area Walkdowns=== | ===.1 Fire Area Walkdowns=== | ||
The inspectors toured the following six plant areas to evaluate conditions related to control of transient combustibles and ignition sources and the material condition and operational status of fire protection systems including fire barriers used to prevent fire damage and propagation. The inspectors reviewed these activities using provisions in the licensees procedure 0-ADM-016, Fire Protection Plan, and 10 CFR Part 50, Appendix R. The licensees fire impairment lists were routinely reviewed. In addition, the inspectors reviewed the condition report database to verify that fire protection problems were being identified and appropriately resolved. The following areas were inspected: | The inspectors toured the following six plant areas to evaluate conditions related to control of transient combustibles and ignition sources and the material condition and operational status of fire protection systems including fire barriers used to prevent fire damage and propagation. The inspectors reviewed these activities using provisions in the licensees procedure 0-ADM-016, Fire Protection Plan, and 10 CFR Part 50, Appendix R. The licensees fire impairment lists were routinely reviewed. In addition, the inspectors reviewed the condition report database to verify that fire protection problems were being identified and appropriately resolved. The following areas were inspected: | ||
* 3A emergency diesel generator room | * 3A emergency diesel generator room | ||
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===.2 Annual Fire Drill=== | ===.2 Annual Fire Drill=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On April 20 and again on May 20, 2010, the inspectors observed the licensee fire brigades response to a simulated fire on the control room roof. Two groups of responders were observed, one on each occasion. The inspectors verified that control room communications with the fire brigade were established and announcement of the fire location and sounding of alarms were made in a timely manner. The inspectors verified that the drill was administered in accordance with licensee procedures FPAD-027, Fire Brigade and Mutual Aid Drill Scenario Development and 0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions. The inspectors checked the brigades communications, ability to set-up and execute fire operations, and their use of fire fighting equipment. The inspectors verified that the licensee implemented the aspects as described below when the brigade simulated the firefighting activities during the post-drill critique. | On April 20 and again on May 20, 2010, the inspectors observed the licensee fire brigades response to a simulated fire on the control room roof. Two groups of responders were observed, one on each occasion. The inspectors verified that control room communications with the fire brigade were established and announcement of the fire location and sounding of alarms were made in a timely manner. The inspectors verified that the drill was administered in accordance with licensee procedures FPAD-027, Fire Brigade and Mutual Aid Drill Scenario Development and 0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions. The inspectors checked the brigades communications, ability to set-up and execute fire operations, and their use of fire fighting equipment. The inspectors verified that the licensee implemented the aspects as described below when the brigade simulated the firefighting activities during the post-drill critique. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R06}} | No findings were identified. {{a|1R06}} | ||
==1R06 Flood Protection Measures | |||
==1R06 Flood Protection Measures | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors conducted walkdowns of the following two areas subject to internal flooding to ensure that flood protection measures were in accordance with design specifications. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), Appendix 5F, Internal Plant Flooding that discussed protection of areas containing safety-related equipment that could be affected by internal flooding. Specific plant attributes that were checked included structural integrity, sealing of penetrations and control of debris. Operability of sump systems including alarms was verified by review of completed licensee procedure 0-PMI-065.05, Residual Heat Removal Room Sump Functional Test. Manhole inspections were completed, including checking for accumulated water and cable integrity problems. When water was identified in manhole 403, the inspectors verified that safety related components were of the appropriate design and that safety was not adversely affected. | The inspectors conducted walkdowns of the following two areas subject to internal flooding to ensure that flood protection measures were in accordance with design specifications. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), Appendix 5F, Internal Plant Flooding that discussed protection of areas containing safety-related equipment that could be affected by internal flooding. Specific plant attributes that were checked included structural integrity, sealing of penetrations and control of debris. Operability of sump systems including alarms was verified by review of completed licensee procedure 0-PMI-065.05, Residual Heat Removal Room Sump Functional Test. Manhole inspections were completed, including checking for accumulated water and cable integrity problems. When water was identified in manhole 403, the inspectors verified that safety related components were of the appropriate design and that safety was not adversely affected. | ||
* Unit 3 Residual Heat Removal (RHR) Pump Rooms | * Unit 3 Residual Heat Removal (RHR) Pump Rooms | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R11}} | No findings were identified. {{a|1R11}} | ||
==1R11 Licensed Operator Requalification Program | |||
== | |||
===.1 Resident Inspector Quarterly Review=== | ===.1 Resident Inspector Quarterly Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On June 10, 2010, the inspectors observed and assessed licensed operator performance in the plant specific simulator. The simulated events were done using Emergency Preparedness Second Quarter Drill which involved a simulated loss of control room annunciators for more than 15 minutes, a lockout of safety electrical bus 3B, a fire in the Unit 3 auxiliary transformer, and a steam generator tube rupture. | On June 10, 2010, the inspectors observed and assessed licensed operator performance in the plant specific simulator. The simulated events were done using Emergency Preparedness Second Quarter Drill which involved a simulated loss of control room annunciators for more than 15 minutes, a lockout of safety electrical bus 3B, a fire in the Unit 3 auxiliary transformer, and a steam generator tube rupture. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R12}} | No findings were identified. {{a|1R12}} | ||
==1R12 Maintenance Effectiveness | |||
==1R12 Maintenance Effectiveness | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed the following two equipment problems and associated condition reports to verify that the licensees maintenance efforts met the requirements of 10 CFR 50.65 (Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants) and licensee administrative procedure 0-ADM-728, Maintenance Rule Implementation. The inspectors efforts focused on maintenance rule scoping, characterization of maintenance problems and failed components, risk significance, determination of a(1) classification, corrective actions, and the appropriateness of established performance goals and monitoring criteria. The inspectors also interviewed responsible engineers and observed some of the corrective maintenance activities. The inspectors verified that equipment problems were being identified and entered into the corrective action program. The inspectors used licensee maintenance rule data base, system health reports, and the corrective action program as sources of information on tracking and resolution of issues. | The inspectors reviewed the following two equipment problems and associated condition reports to verify that the licensees maintenance efforts met the requirements of 10 CFR 50.65 (Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants) and licensee administrative procedure 0-ADM-728, Maintenance Rule Implementation. The inspectors efforts focused on maintenance rule scoping, characterization of maintenance problems and failed components, risk significance, determination of a(1) classification, corrective actions, and the appropriateness of established performance goals and monitoring criteria. The inspectors also interviewed responsible engineers and observed some of the corrective maintenance activities. The inspectors verified that equipment problems were being identified and entered into the corrective action program. The inspectors used licensee maintenance rule data base, system health reports, and the corrective action program as sources of information on tracking and resolution of issues. | ||
* CR 2010-8402, 3A qualified safety parameter display system (QSPDS), reactor vessel level temperature element TE-3-6493 failed requiring entry into the 30 day technical specification action. System Health Report for System 42, QSPDS, dated March 31, 2010, which included the a(1) action plan was reviewed. | * CR 2010-8402, 3A qualified safety parameter display system (QSPDS), reactor vessel level temperature element TE-3-6493 failed requiring entry into the 30 day technical specification action. System Health Report for System 42, QSPDS, dated March 31, 2010, which included the a(1) action plan was reviewed. | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R13}} | No findings were identified. {{a|1R13}} | ||
==1R13 Maintenance Risk Assessments and Emergent Work Control | |||
==1R13 Maintenance Risk Assessments and Emergent Work Control | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors completed in-office reviews and control room inspections of the licensees risk assessment of six emergent or planned maintenance activities. The inspectors verified the licensees risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and Procedures 0-ADM-068, Work Week Management and O-ADM-225, On Line Risk Assessment and Management. The inspectors also reviewed the effectiveness of the licensees contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee assessment of aggregate risk using FPL procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors evaluated the following risk assessments during the inspection: | The inspectors completed in-office reviews and control room inspections of the licensees risk assessment of six emergent or planned maintenance activities. The inspectors verified the licensees risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and Procedures 0-ADM-068, Work Week Management and O-ADM-225, On Line Risk Assessment and Management. The inspectors also reviewed the effectiveness of the licensees contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee assessment of aggregate risk using FPL procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors evaluated the following risk assessments during the inspection: | ||
* April 9, risk management during recovery from maintenance on heater drain valve 4-1510A | * April 9, risk management during recovery from maintenance on heater drain valve 4-1510A | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R15}} | No findings were identified. {{a|1R15}} | ||
==1R15 Operability Evaluations | |||
==1R15 Operability Evaluations | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
For the five operability evaluations described in the condition reports (CR) listed below, the inspectors evaluated the technical adequacy of licensee evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors reviewed the final safety analysis report to verify that the system or component remained available to perform its intended function. In addition, when applicable, the inspectors reviewed compensatory measures implemented to verify that the plant design basis was being maintained. The inspectors also reviewed a sampling of condition reports to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. | For the five operability evaluations described in the condition reports (CR) listed below, the inspectors evaluated the technical adequacy of licensee evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors reviewed the final safety analysis report to verify that the system or component remained available to perform its intended function. In addition, when applicable, the inspectors reviewed compensatory measures implemented to verify that the plant design basis was being maintained. The inspectors also reviewed a sampling of condition reports to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations. | ||
* CR 2010-9904, Standby Steam Generator Feed Pump B trouble alarm locked in without reflash due to alarm circuit issues | * CR 2010-9904, Standby Steam Generator Feed Pump B trouble alarm locked in without reflash due to alarm circuit issues | ||
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====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R17}} | No findings were identified. {{a|1R17}} | ||
==== | ==1R17 Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications | ||
a. | |||
== | |||
Inspection Scope | |||
The inspectors reviewed selected samples of evaluations to confirm that the licensee had appropriately considered the conditions under which changes to the facility, Updated Final Safety Analysis Report (UFSAR), or procedures may be made, and tests conducted, without prior NRC approval. The inspectors reviewed evaluations for eight changes and additional information, such as drawings, calculations, supporting analyses, the UFSAR, and Technical Specifications (TS) to confirm that the licensee had appropriately concluded that the changes could be accomplished without obtaining a license amendment. The eight evaluations reviewed are listed in the List of Documents Reviewed. | The inspectors reviewed selected samples of evaluations to confirm that the licensee had appropriately considered the conditions under which changes to the facility, Updated Final Safety Analysis Report (UFSAR), or procedures may be made, and tests conducted, without prior NRC approval. The inspectors reviewed evaluations for eight changes and additional information, such as drawings, calculations, supporting analyses, the UFSAR, and Technical Specifications (TS) to confirm that the licensee had appropriately concluded that the changes could be accomplished without obtaining a license amendment. The eight evaluations reviewed are listed in the List of Documents Reviewed. | ||
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* PCN 08-012, CS Pump Material Changes | * PCN 08-012, CS Pump Material Changes | ||
* PCN 07-087, 4B DOST Sample Valve ADDN | * PCN 07-087, 4B DOST Sample Valve ADDN | ||
* PCN 08-151, Unit 3 EDG Day Tank Level Switches Setpoint Change Documents reviewed included procedures, engineering calculations, modification design and implementation packages, work orders, site drawings, corrective action documents, applicable sections of the living UFSAR, supporting analyses, TS, and design basis information. The inspectors additionally reviewed test documentation to ensure adequacy in scope and conclusion. The inspectors review was also intended to verify that all details were incorporated in licensing and design basis documents and associated plant procedures. | * PCN 08-151, Unit 3 EDG Day Tank Level Switches Setpoint Change | ||
Documents reviewed included procedures, engineering calculations, modification design and implementation packages, work orders, site drawings, corrective action documents, applicable sections of the living UFSAR, supporting analyses, TS, and design basis information. The inspectors additionally reviewed test documentation to ensure adequacy in scope and conclusion. The inspectors review was also intended to verify that all details were incorporated in licensing and design basis documents and associated plant procedures. | |||
The inspectors also reviewed selected condition reports and the licensees recent self-assessment associated with modifications and screening/evaluation issues to confirm that problems were identified at an appropriate threshold, were entered into the corrective action process, and appropriate corrective actions had been initiated and tracked to completion. | The inspectors also reviewed selected condition reports and the licensees recent self-assessment associated with modifications and screening/evaluation issues to confirm that problems were identified at an appropriate threshold, were entered into the corrective action process, and appropriate corrective actions had been initiated and tracked to completion. | ||
| Line 276: | Line 353: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R18}} | No findings were identified. {{a|1R18}} | ||
==1R18 Plant Modifications | |||
==1R18 Plant Modifications | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors reviewed the two temporary system modifications and one permanent plant modification listed below to ensure that that the modifications did not adversely affect safety system availability or reliability. The inspectors reviewed plant modifications for systems that were ranked high in risk for departures from design basis and for inadvertent changes that could challenge the systems to fulfill their safety function. For the permanent modification, the inspectors reviewed the licensees 10 CFR 50.59 screening to assure that NRC approval was not required prior to installation of the modification. The inspectors specifically checked material compatibility of added components, seismic qualification, adverse containment effects, and structural integrity. | The inspectors reviewed the two temporary system modifications and one permanent plant modification listed below to ensure that that the modifications did not adversely affect safety system availability or reliability. The inspectors reviewed plant modifications for systems that were ranked high in risk for departures from design basis and for inadvertent changes that could challenge the systems to fulfill their safety function. For the permanent modification, the inspectors reviewed the licensees 10 CFR 50.59 screening to assure that NRC approval was not required prior to installation of the modification. The inspectors specifically checked material compatibility of added components, seismic qualification, adverse containment effects, and structural integrity. | ||
| Line 288: | Line 367: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R19}} | No findings were identified. {{a|1R19}} | ||
==1R19 Post Maintenance Testing | |||
==1R19 Post Maintenance Testing | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
For the five post maintenance tests listed below, the inspectors reviewed the test procedures and either witnessed the testing and/or reviewed test records to determine whether the scope of testing adequately verified that the work performed was correctly completed and demonstrated that the affected equipment was operable. The inspectors used licensee procedure 0-ADM-737, Post Maintenance Testing, in their assessments. | For the five post maintenance tests listed below, the inspectors reviewed the test procedures and either witnessed the testing and/or reviewed test records to determine whether the scope of testing adequately verified that the work performed was correctly completed and demonstrated that the affected equipment was operable. The inspectors used licensee procedure 0-ADM-737, Post Maintenance Testing, in their assessments. | ||
* Unit 4: Satisfactory leak check under work order 40007951, following repair of a lubricating oil leak on the 4A emergency diesel generator (4K4A) main pressure pump discharge line (CR 2010-11424) | * Unit 4: Satisfactory leak check under work order 40007951, following repair of a lubricating oil leak on the 4A emergency diesel generator (4K4A) main pressure pump discharge line (CR 2010-11424) | ||
| Line 300: | Line 381: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. {{a|1R22}} | No findings were identified. {{a|1R22}} | ||
==1R22 Surveillance Testing | |||
==1R22 Surveillance Testing | |||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
== | |||
The inspectors either reviewed or witnessed the following six surveillance tests to verify that the tests met the technical specification requirements, the UFSAR, and the licensees procedural requirements and demonstrated that the systems were operationally ready to perform their intended safety functions. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the positions/status required for the system to perform its safety function. Two inservice testings (IST) were validated using the licensees Inservice Testing Program Fourth Ten Year Interval, dated March 11, 2004. | The inspectors either reviewed or witnessed the following six surveillance tests to verify that the tests met the technical specification requirements, the UFSAR, and the licensees procedural requirements and demonstrated that the systems were operationally ready to perform their intended safety functions. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the positions/status required for the system to perform its safety function. Two inservice testings (IST) were validated using the licensees Inservice Testing Program Fourth Ten Year Interval, dated March 11, 2004. | ||
| Line 314: | Line 397: | ||
====b. Findings==== | ====b. Findings==== | ||
No findings were identified. | No findings were identified. | ||
===Cornerstone: Emergency Preparedness=== | ===Cornerstone: Emergency Preparedness=== | ||
1EP6 Drill Evaluation | 1EP6 Drill Evaluation | ||
===.1 Simulator Based Training Evolution=== | ===.1 Simulator Based Training Evolution=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
On June 10, 2010, the inspectors observed an operating crew in the plant simulator and technical support center (TSC) staff during the second quarter emergency plan drill of the site emergency response organization. The drill included a loss of plant annunciators and declaration of an Unusual Event. Subsequently, a ground was simulated on the 3B 4160 volt safety bus resulting in loss of the bus with an accompanying reactor trip. A fire in the auxiliary transformer resulted in an alert declaration. The inspectors verified proper staffing of the emergency response facilities. | On June 10, 2010, the inspectors observed an operating crew in the plant simulator and technical support center (TSC) staff during the second quarter emergency plan drill of the site emergency response organization. The drill included a loss of plant annunciators and declaration of an Unusual Event. Subsequently, a ground was simulated on the 3B 4160 volt safety bus resulting in loss of the bus with an accompanying reactor trip. A fire in the auxiliary transformer resulted in an alert declaration. The inspectors verified proper staffing of the emergency response facilities. | ||
| Line 332: | Line 413: | ||
==RADIATION SAFETY== | ==RADIATION SAFETY== | ||
{{a|2RS8}} | {{a|2RS8}} | ||
==2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and== | ==2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and== | ||
Transportation | Transportation | ||
| Line 340: | Line 421: | ||
====b. Findings==== | ====b. Findings==== | ||
=====Introduction:===== | =====Introduction:===== | ||
The inspectors identified a Green non-cited violation (NCV) of 10 CFR Part 20.1501(a) for the failure to perform adequate surveys to meet the requirements of 10 CFR Part 20 Appendix G which states that shippers of radioactive waste must identify and quantify radionuclides contained in each waste container. Specifically, the inspectors determined that the use of resin samples to characterize shipments of mechanical filters was inadequate to ensure proper identification and quantification of the radionuclides present in each container. | The inspectors identified a Green non-cited violation (NCV) of 10 CFR Part 20.1501(a) for the failure to perform adequate surveys to meet the requirements of 10 CFR Part 20 Appendix G which states that shippers of radioactive waste must identify and quantify radionuclides contained in each waste container. Specifically, the inspectors determined that the use of resin samples to characterize shipments of mechanical filters was inadequate to ensure proper identification and quantification of the radionuclides present in each container. | ||
| Line 363: | Line 443: | ||
==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
{{a|4OA2}} | {{a|4OA2}} | ||
==4OA2 Problem Identification and Resolution== | ==4OA2 Problem Identification and Resolution== | ||
===.1 Daily Review=== | ===.1 Daily Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensees corrective action program. This review was accomplished by reviewing daily summaries of condition reports and by reviewing the licensees electronic condition report database. Additionally, a reactor coolant system unidentified leakage was checked on a daily basis to verify no substantive or unexplained changes. | As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensees corrective action program. This review was accomplished by reviewing daily summaries of condition reports and by reviewing the licensees electronic condition report database. Additionally, a reactor coolant system unidentified leakage was checked on a daily basis to verify no substantive or unexplained changes. | ||
| Line 374: | Line 453: | ||
===.2 Annual Sample Review=== | ===.2 Annual Sample Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors selected the following two condition reports for detailed review and discussion with the licensee. The condition reports were reviewed to ensure that an appropriate evaluation was performed and appropriate corrective actions were specified and prioritized. Other attributes checked included disposition of operability and resolution of the problem including cause determination and corrective actions. The inspectors evaluated the condition reports in accordance with the requirements of the licensees corrective actions process as specified in licensee procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action. The inspectors reviewed the cumulative effects of the operator workarounds that were in place to verify that those effects could not increase an initiating event frequency, affect multiple mitigating systems, or affect the ability of operators to properly respond to plant transients and accidents. The inspectors also reviewed operator workarounds to verify that the licensee was identifying operator workaround problems at an appropriate threshold and entering them in the corrective action program. | The inspectors selected the following two condition reports for detailed review and discussion with the licensee. The condition reports were reviewed to ensure that an appropriate evaluation was performed and appropriate corrective actions were specified and prioritized. Other attributes checked included disposition of operability and resolution of the problem including cause determination and corrective actions. The inspectors evaluated the condition reports in accordance with the requirements of the licensees corrective actions process as specified in licensee procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action. The inspectors reviewed the cumulative effects of the operator workarounds that were in place to verify that those effects could not increase an initiating event frequency, affect multiple mitigating systems, or affect the ability of operators to properly respond to plant transients and accidents. The inspectors also reviewed operator workarounds to verify that the licensee was identifying operator workaround problems at an appropriate threshold and entering them in the corrective action program. | ||
| Line 384: | Line 462: | ||
===.3 Semi-Annual Trend Review=== | ===.3 Semi-Annual Trend Review=== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
As required by Inspection Procedure 71152, Identification and Resolution of Problems, the inspectors reviewed the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector corrective actions item screening discussed in section 4OA2.1 above, plant status reviews, plant tours, document reviews, and licensee trending efforts. Among the documents reviewed was the Turkey Point Station Performance Improvement Health Report, 1st Quarter 2010, dated May 14, 2010. The inspectors review nominally considered the six month period of January through June 2010. Corrective actions associated with a sample of the issues identified in the licensees corrective action program were reviewed for adequacy. | As required by Inspection Procedure 71152, Identification and Resolution of Problems, the inspectors reviewed the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector corrective actions item screening discussed in section 4OA2.1 above, plant status reviews, plant tours, document reviews, and licensee trending efforts. Among the documents reviewed was the Turkey Point Station Performance Improvement Health Report, 1st Quarter 2010, dated May 14, 2010. The inspectors review nominally considered the six month period of January through June 2010. Corrective actions associated with a sample of the issues identified in the licensees corrective action program were reviewed for adequacy. | ||
b. Assessment and Observations No findings were identified. . | b. | ||
Assessment and Observations | |||
No findings were identified.. | |||
{{a|4OA3}} | {{a|4OA3}} | ||
==4OA3 Follow-up of Events== | ==4OA3 Follow-up of Events== | ||
====a. Inspection Scope==== | ====a. Inspection Scope==== | ||
The inspectors reviewed the licensees personnel performance during an unplanned trip | The inspectors reviewed the licensees personnel performance during an unplanned trip of the Unit 3 B condensate pump resulting in power reduction on June 3, 2010. | ||
====b. Findings==== | ====b. Findings==== | ||
=====Introduction:===== | =====Introduction:===== | ||
(Green) A Self-Revealing Non-cited Violation of Technical Specification requirements was identified when rod position indication for two rod control cluster assemblies (RCCs) drifted out of tolerance with the associated rod group position indication. Contrary to technical specification requirements, rod positions were neither re-aligned with the group counter nor was reactor power reduced to less than 90 percent within the specified one hour action time. | (Green) A Self-Revealing Non-cited Violation of Technical Specification requirements was identified when rod position indication for two rod control cluster assemblies (RCCs) drifted out of tolerance with the associated rod group position indication. Contrary to technical specification requirements, rod positions were neither re-aligned with the group counter nor was reactor power reduced to less than 90 percent within the specified one hour action time. | ||
| Line 418: | Line 499: | ||
{{a|4OA6}} | {{a|4OA6}} | ||
==4OA6 Exit== | ==4OA6 Exit== | ||
===Exit Meeting Summary=== | ===Exit Meeting Summary=== | ||
The resident inspectors presented the inspection results to Mr. Kiley and other members of licensee management on July 19, 2010. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information. | The resident inspectors presented the inspection results to Mr. Kiley and other members of licensee management on July 19, 2010. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information. | ||
ATTACHMENT: SUPPPLEMENTAL INFORMATION | ATTACHMENT: SUPPPLEMENTAL INFORMATION | ||
=SUPPLEMENTAL INFORMATION= | =SUPPLEMENTAL INFORMATION= | ||
==KEY POINTS OF CONTACT== | ==KEY POINTS OF CONTACT== | ||
===Licensee personnel=== | |||
: | |||
: [[contact::N. Bach]], Chemistry Manager | |||
: [[contact::C. Cashwell]], Radiation Protection Manager | |||
: [[contact::R. Coffey]], Maintenance Manager | |||
: [[contact::M. Crosby]], Quality Manager | |||
: [[contact::J. Garcia]], Engineering Manager | |||
: [[contact::M. Epstein]], Emergency Preparedness Manager (Acting) | |||
: [[contact::M. Kiley]], Site Vice-President | |||
: [[contact::J. Patterson]], Fire Protection Supervisor | |||
: [[contact::P. Rubin]], Plant General Manager | |||
: [[contact::R. Tomonto]], Licensing Manager | |||
: [[contact::S. Shafer]], Assistant Operations Manager | |||
: [[contact::R. Wright]], Operations Manager | |||
===NRC personnel=== | ===NRC personnel=== | ||
: | : | ||
: [[contact::L. Wert]], Director, Division of Reactor Projects | : [[contact::L. Wert]], Director, Division of Reactor Projects | ||
: [[contact::M. Sykes]], Chief, Reactor Projects Branch 3 | : [[contact::M. Sykes]], Chief, Reactor Projects Branch 3 | ||
==LIST OF ITEMS== | ==LIST OF ITEMS== | ||
===OPENED, CLOSED AND DISCUSSED=== | ===OPENED, CLOSED AND DISCUSSED=== | ||
===Closed=== | |||
: 05000250, 251/2009-05-02 | |||
URI Inappropriate characterization of RCS filters for transportation and disposal (Section 2RS8) | |||
===Opened and Closed=== | ===Opened and Closed=== | ||
: 05000250, 251/2010-03-01 | : 05000250, 251/2010-03-01 NCV Failure to perform adequate surveys to ensure proper estimation of radionuclide concentrations in mechanical filter waste shipments (Section 2RS8) | ||
: 05000250, 251/2010-03-02 | : 05000250, 251/2010-03-02 NCV Failure to implement TS requirements regarding | ||
rod position indication (Section 4OA3) | |||
==LIST OF DOCUMENTS== | ==LIST OF DOCUMENTS== | ||
/DATA REVIEWED | /DATA REVIEWED | ||
}} | }} | ||
Latest revision as of 03:49, 14 January 2025
| ML102100318 | |
| Person / Time | |
|---|---|
| Site: | Turkey Point |
| Issue date: | 07/28/2010 |
| From: | Rich D NRC/RGN-II/DRP/RPB3 |
| To: | Nazar M Florida Power & Light Co |
| References | |
| IR-10-003 | |
| Download: ML102100318 (31) | |
Text
July 28, 2010
SUBJECT:
TURKEY POINT NUCLEAR PLANT - INTEGRATED INSPECTION REPORT 05000250/2010003 AND 05000251/2010003
Dear Mr. Nazar:
On June 30, 2010, the US Nuclear Regulatory Commission (NRC) completed an inspection at your Turkey Point Units 3 and 4. The enclosed inspection report documents the inspection results, which were discussed on July 19, 2010, with Mr. Kiley and other members of your staff.
The inspection examined activities conducted under your license as they related to safety and compliance with the Commissions rules and regulations and with the conditions of your license.
The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel.
The report documents one NRC identified and one self-revealing finding of very low safety significance (Green). These findings were determined to involve violations of NRC requirements. However, because of very low safety significance and because they are entered into your corrective action program, the NRC is treating these findings as non-cited violations (NCVs) consistent with Section VI.A.1 of the NRC Enforcement Policy. If you contest any NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN.: Document Control Desk, Washington DC 20555-001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at Turkey Point. In addition, if you disagree with the characterization of any finding in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II, and the NRC Resident Inspector at Turkey Point.
In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of the NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Daniel W. Rich, Chief
Rector Projects Branch 3
Division of Reactor Projects
Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41
Enclosure:
Inspection Report 05000250/2010003 and 05000251/2010003
w/Attachment: Supplemental Information
__ML102100318________________
X SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRS RII:DRS RII:DRP RII:DRS RII:DRS SIGNATURE SON JSS1 by email AND by email GBK1 by email JBH4 by email JAE1 by email AXA1 by email NAME SNinh JStewart ANielsen GKuzo JHamman JEargle AAlen DATE 0728/2010 07/27/2010 07/21/2010 07/21/2010 07/26/2010 07/23/2010 07/27/2010 E-MAIL COPY?
YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:DRP
SIGNATURE MCB by email
NAME MBarillas
DATE 07/26/2010
E-MAIL COPY?
YES NO YES NO YES NO YES NO YES NO YES NO YES NO
REGION II==
Docket Nos.:
50-250, 50-251
License Nos.:
Report No:
05000250/2010003, 05000251/2010003
Licensee:
Florida Power & Light Company (FP&L)
Facility:
Turkey Point Nuclear Plant, Units 3 & 4
Location:
9760 S. W. 344th Street Homestead, FL 33035
Dates:
April 1 to June 30, 2010
Inspectors:
J. Stewart, Senior Resident Inspector
M. Barillas, Resident Inspector A. Nielsen, Health Physicist (2RS8)
G. Kuzo, Senior Health Physicist (2RS8)
J. Hamman, Reactor Inspector (1R17)
S. Ninh, Senior Project Engineer (1R17)
J. Eargle, Reactor Inspector (1R17)
A. Alen, Reactor Inspector (1R17)
Approved by:
D. Rich, Branch, Chief Reactor Projects Branch 3 Division of Reactor Projects
Enclosure
SUMMARY OF FINDINGS
IR 05000250/2010-003, 05000251/2010-003; 4/1/2010 - 6/30/2010; Turkey Point Nuclear
Power Plant, Units 3 and 4; Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and Transportation, Followup of Events
The report covered a three month period of inspection by resident inspectors and region based health physicists. Two Green NCVs were identified. The significance of most findings is identified by their color (Green, White, Yellow, Red) using IMC 0609, Significance Determination Process (SDP); the cross-cutting aspect was determined using IMC 305,
Operating Reactor Assessment Program; and that findings for which the SDP does not apply may be Green or be assigned a severity level after NRC management review. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December, 2006.
NRC-Identified
& Self-Revealing Findings
Cornerstone: Initiating Events
- Green.
A Self-Revealing Non-cited Violation of Technical Specification 3.1.3.1.b requirements was identified on Unit 3 when position indication for two rod control cluster assemblies (RCCs) drifted out of tolerance with the associated rod group position indication.
Contrary to technical specification requirements, rod positions were neither re-aligned with the group counter nor was reactor power reduced to less than 90 percent within the allowed one hour action time with a potential consequence of challenging accident analysis assumptions. The issue was documented in the corrective action program as CR 2010-14724.
The finding was more than minor because if inaccurate rod position indication was left uncorrected, there was a possibility of an adverse affect of an actual rod misalignment beyond that assumed in accident analyses. The Initiating Events cornerstone was affected because rod position alignment assures that accident analysis assumptions are maintained.
The inspectors evaluated the finding using NRC Inspection Manual 0609, Attachment 0609.04, Initial Screening and Characterization of Findings and classified the finding of very low safety significance (Green) using the Transient Initiator tool. The cross-cutting aspect of Human Performance, Decision Making (H.1.a) was affected when supervisory personnel did not implement their roles and authorities to ensure safety by implementing Technical Specification requirements. (4OA3)
Cornerstone: Public Radiation Safety (RS)
- Green The inspectors identified a Green non-cited violation (NCV) of 10 CFR Part 20.1501(a) for the failure to perform adequate surveys to meet the requirements of 10 CFR Part 20 Appendix G. 10 CFR Part 20 Appendix G states that shippers of radioactive waste must identify and quantify radionuclides contained in each waste container. Specifically, the inspectors determined that the use of resin samples to characterize three shipments of mechanical filters in calendar years 2008 and 2009 was inadequate to ensure proper identification and quantification of the radionuclides present in each container. The licensee entered the issue into their corrective action program as condition report (CR) number 2009-32955.
The finding is more than minor because it is associated with the Public Radiation Safety cornerstone attribute of Programs and Processes and adversely affects the cornerstone objective of ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. The finding was assessed using the Public Radiation Safety Significance Determination Process (SDP). Based on the fact that subsequent follow up analyses demonstrated that none of the filter waste was under-classified, the finding was determined to be of very low safety significance (Green). This finding has a crosscutting aspect of Human Performance, Decision Making H.1(b), because the decision to use resin samples to characterize filter shipments was based on incorrect assumptions, i.e., that spent resin samples would be representative of the filter waste stream, and those assumptions were not demonstrated to be conservative prior to implementation. (Section 2RS8)
Licensee Identified Violations
None
REPORT DETAILS
Summary of Plant Status:
Unit 3: Unit 3 started the period at full power. Reactor power was reduced to 90 percent on June 23 to repair a secondary system pump then returned to full power on June 24 and was at full power for the rest of the inspection period.
Unit 4 operated at full power throughout the inspection period.
REACTOR SAFETY
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity (Reactor-R)
1R01 Adverse Weather Protection (02.01 Summer Readiness of Offsite and Alternate AC
Power Systems, 02.02 Readiness for Extreme Weather Conditions, and 02.04 Readiness to Cope with External Flooding)
a. Inspection Scope
During the week of May 24, the inspectors reviewed and verified the status of licensee actions in preparation for hot weather and hurricane season. The inspectors reviewed licensee procedures 0-ONOP-103.3, Severe Weather Preparations; 0-ADM-116, Hurricane Season Preparation; 0-ADM-216, PTN and PTF Shared System Work Control and Switchyard Access; 0-SMM-102.1, Flood Protection Stoplog and Penetration Seal Inspection; 0-EPIP-20106, Natural Emergencies; and 0-EPIP-20101, Duties of Emergency Coordinator in making their assessment. Licensee procedure 0-ONOP-004.6, Degraded Switchyard Voltage, was reviewed and discussed with operators to assure that actions planned if switchyard voltage was outside of limits or could not be predicted (post-trip) were appropriate. Licensee procedure 0-ADM-225, Online Risk Assessment and Management was reviewed to verify that appropriate actions were specified for risk management of degraded grid conditions. The inspectors performed site walk downs and tours of vulnerable areas (listed below) to verify that no activities would prevent the licensee from making timely storm preparations, if needed. The inspectors reviewed the Hurricane Season Preparation open items list and verified that the open exemptions were being documented in the corrective action program with a plan to correct them prior to a hurricane event. The following areas of the site were specifically inspected:
- Unit 3 and Unit 4 C bus transformer areas (02.01)
- Unit 3 and Unit 4 startup transformers (02.01)
- Main switchyard (02.02)
- Intake area (02.02)
- Unit 3 4160 volt switchgear rooms (02.02, 02.04)
- Unit 3 and unit 4 spent fuel cooling pump rooms (02.04)
b. Findings
No findings were identified.
==1R01 Adverse Weather Protection (02.03, Evaluate Readiness for Impending Adverse Weather Conditions)
==
a. Inspection Scope
The inspectors evaluated the implementation of off-normal procedure 0-ONOP-011.1, Intake Canal High Temperature when the intake cooling water exceeded 96 degrees F which coincided with high containment ambient temperatures during the week of June 14. The inspectors verified that Technical Specification 3.6.1.5 high temperature equivalent hours were recorded and tracked.
b. Findings
No findings were identified.
==1R04 Equipment Alignment
==
.1 Partial Equipment Walkdowns
a. Inspection Scope
The inspectors conducted three partial alignment verifications of the safety-related systems listed below. These inspections included reviews using operating procedures and piping and instrumentation drawings, which were compared with observed equipment configurations to verify that the critical portions of the systems were correctly aligned to support operability. The inspectors also verified that the licensee had identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems. The inspectors routinely verified that alignment issues were documented in the corrective action program.
- Unit 4, High head safety injection alignment (outside containment) using licensee procedure 4-NOP-062, Safety Injection, following venting performed due to gas intrusion (CR 2010-9497, CR 2010-7918) April 13, 2010
- Unit 4, 4B Emergency Diesel Generator and the station blackout cross-tie when 4A EDG was removed from service for maintenance overhaul. The walkdown was done using licensee lineups specified in 4-OP-023, Emergency Diesel Generator
- Unit 3 and Unit 4, Equipment Operability Verification with An Emergency Diesel Generator Inoperable, 0-OSP-023.3, when 3B EDG diesel oil transfer pump failed to auto start on June 7, 2010
b. Findings
No findings were identified.
.2 Complete System Walkdown
a. Inspection Scope
The inspectors performed a detailed review of the alignment and condition of system 062, Unit 4 safety injection, to verify that the existing alignment was consistent with the design. To determine the correct system alignment, the inspectors reviewed Turkey Point Technical Specifications (TS); licensee procedure 4-OSP-202.1, Safety Injection Flowpath Verification; procedure 4-NOP-062, Unit 4 Safety Injection; piping and instrumentation drawing 5614-M-3062; the design basis document; and the FSAR. The inspectors walked down supports and restraints associated with selected piping of the safety injection pumps. During the walkdown, the inspectors reviewed the following:
- Valves were correctly positioned and did not exhibit leakage that would impact the functions of any given valve. The inspectors verified that dry boric acid was logged and had a work request associated with the component.
- Electrical power was available as required.
- Major system components were correctly labeled, lubricated, cooled, ventilated, etc.
- Hangers and supports were correctly installed and functional.
- Essential support systems were operational.
- Ancillary equipment or debris did not interfere with system performance.
- Tagging clearances were appropriate.
- Valves were locked as required by the locked valve program.
Design and equipment issues were reviewed to determine if the identified deficiencies significantly impacted the systems functions. Items included in this review were the temporary modifications, system health report, the system description, pump vibration data, condition reports, and outstanding maintenance work orders (WOs). In addition, the inspectors reviewed the licensees corrective action program to ensure that the licensee was identifying and resolving equipment alignment problems in a timely manner.
b. Findings
No findings were identified.
==1R05 Fire Protection
a. Inspection Scope
==
.1 Fire Area Walkdowns
The inspectors toured the following six plant areas to evaluate conditions related to control of transient combustibles and ignition sources and the material condition and operational status of fire protection systems including fire barriers used to prevent fire damage and propagation. The inspectors reviewed these activities using provisions in the licensees procedure 0-ADM-016, Fire Protection Plan, and 10 CFR Part 50, Appendix R. The licensees fire impairment lists were routinely reviewed. In addition, the inspectors reviewed the condition report database to verify that fire protection problems were being identified and appropriately resolved. The following areas were inspected:
- 3A emergency diesel generator room
- Auxiliary building breezeway
- Main control room
- 3B emergency diesel generator room
- Unit 3 charging pump room
- Auxiliary building hallway
b. Findings
No findings were identified.
.2 Annual Fire Drill
a. Inspection Scope
On April 20 and again on May 20, 2010, the inspectors observed the licensee fire brigades response to a simulated fire on the control room roof. Two groups of responders were observed, one on each occasion. The inspectors verified that control room communications with the fire brigade were established and announcement of the fire location and sounding of alarms were made in a timely manner. The inspectors verified that the drill was administered in accordance with licensee procedures FPAD-027, Fire Brigade and Mutual Aid Drill Scenario Development and 0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions. The inspectors checked the brigades communications, ability to set-up and execute fire operations, and their use of fire fighting equipment. The inspectors verified that the licensee implemented the aspects as described below when the brigade simulated the firefighting activities during the post-drill critique.
- The brigade, including the fire brigade leader, consisted of a minimum of five team members. On May 20 eight brigade members responded.
- The team members acquired and donned the appropriate turnout gear.
- Self contained breathing apparatus (SCBA) were available and properly donned.
Actual use of breathing air was not done and the inspectors verified that individuals had practiced using air during annual SCBA training.
- Control Room personnel verified and announced the fire location. The fire alarm was sounded and fire brigade personnel were dispatched.
- Fire brigade leader maintained control. Members were briefed (including potential hazards), discussed plan of attack, received assignments, and performed communications checks.
- Fire brigade arrived at the scene in a timely manner, taking the appropriate access route specified in the strategies and procedures.
- Command and control was established near the fire location. Communications were established with the control room personnel.
- Communications were effective between the control room, command post, plant operators and fire brigade response teams.
- Fire hose lines were capable of reaching the fire area; the lines were laid out without flow restrictions and were simulated as being charged. In one case, a fire hose not properly laid out was corrected by the responders.
- The fire brigade arrived with sufficient fire fighting equipment to perform its fire fighting duties. Offsite notification and request for assistance were simulated.
- The drill scenario was followed and the drill acceptance criteria were met.
- A post-drill critique was held to identify strengths and areas for improvement. In one case, operations supervisors did not attend the critique because shift turnover was being conducted.
- All fire-fighting equipment associated with the drill was returned to a state of readiness following completion of the drill.
b. Findings
No findings were identified.
==1R06 Flood Protection Measures
a. Inspection Scope
==
The inspectors conducted walkdowns of the following two areas subject to internal flooding to ensure that flood protection measures were in accordance with design specifications. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR), Appendix 5F, Internal Plant Flooding that discussed protection of areas containing safety-related equipment that could be affected by internal flooding. Specific plant attributes that were checked included structural integrity, sealing of penetrations and control of debris. Operability of sump systems including alarms was verified by review of completed licensee procedure 0-PMI-065.05, Residual Heat Removal Room Sump Functional Test. Manhole inspections were completed, including checking for accumulated water and cable integrity problems. When water was identified in manhole 403, the inspectors verified that safety related components were of the appropriate design and that safety was not adversely affected.
- Unit 3 Residual Heat Removal (RHR) Pump Rooms
- Unit 4 Residual Heat Removal (RHR) Pump Rooms
- Manholes 403 and 731 (direct inspection)
- Manholes 420, 421, 423, 424 (review of records)
b. Findings
No findings were identified.
==1R11 Licensed Operator Requalification Program
==
.1 Resident Inspector Quarterly Review
a. Inspection Scope
On June 10, 2010, the inspectors observed and assessed licensed operator performance in the plant specific simulator. The simulated events were done using Emergency Preparedness Second Quarter Drill which involved a simulated loss of control room annunciators for more than 15 minutes, a lockout of safety electrical bus 3B, a fire in the Unit 3 auxiliary transformer, and a steam generator tube rupture.
Operators responded to the events using off-normal procedure 3-ONOP-097, Loss of Control Room Annunciators; and plant emergency procedures 3-EOP-E-0, Reactor Trip Safety Injection; 3-EOP-ES-0.1, Reactor Trip Response; and 3-ECA-03.1, Steam Generator Tube Rupture, Loss of Reactor Coolant, Subcooled Recovery.
Event classifications (Unusual Event and Alert) were checked for proper classification and simulated state notification in accordance with licensee procedures 0-EPIP-20101, Duties of the Emergency Coordinator; and 0-EPIP-20134, Offsite Notifications and Protective Action Recommendations. The simulator board configurations were compared with actual plant control board configurations concerning recent plant modifications. The inspectors specifically evaluated the following attributes related to operating crew performance and the licensee evaluation:
- Clarity and formality of communication
- Ability to take timely action to safely control the unit
- Prioritization, interpretation, and verification of alarms
- Correct use and implementation of off-normal and emergency operating procedures; and emergency plan implementing procedures
- Control board operation and manipulation, including high-risk operator actions
- Oversight and direction provided by supervision, including ability to identify and implement appropriate TS actions and emergency plan classification and notification
- Crew overall performance and interactions
- Evaluators critique and findings
b. Findings
No findings were identified.
==1R12 Maintenance Effectiveness
a. Inspection Scope
==
The inspectors reviewed the following two equipment problems and associated condition reports to verify that the licensees maintenance efforts met the requirements of 10 CFR 50.65 (Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants) and licensee administrative procedure 0-ADM-728, Maintenance Rule Implementation. The inspectors efforts focused on maintenance rule scoping, characterization of maintenance problems and failed components, risk significance, determination of a(1) classification, corrective actions, and the appropriateness of established performance goals and monitoring criteria. The inspectors also interviewed responsible engineers and observed some of the corrective maintenance activities. The inspectors verified that equipment problems were being identified and entered into the corrective action program. The inspectors used licensee maintenance rule data base, system health reports, and the corrective action program as sources of information on tracking and resolution of issues.
- CR 2010-8402, 3A qualified safety parameter display system (QSPDS), reactor vessel level temperature element TE-3-6493 failed requiring entry into the 30 day technical specification action. System Health Report for System 42, QSPDS, dated March 31, 2010, which included the a(1) action plan was reviewed.
- CR 2008-31372, Unit 4C Main Steam Line snubber failure
b. Findings
No findings were identified.
==1R13 Maintenance Risk Assessments and Emergent Work Control
a. Inspection Scope
==
The inspectors completed in-office reviews and control room inspections of the licensees risk assessment of six emergent or planned maintenance activities. The inspectors verified the licensees risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and Procedures 0-ADM-068, Work Week Management and O-ADM-225, On Line Risk Assessment and Management. The inspectors also reviewed the effectiveness of the licensees contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee assessment of aggregate risk using FPL procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors evaluated the following risk assessments during the inspection:
- April 9, risk management during recovery from maintenance on heater drain valve 4-1510A
- April 28, risk management during maintenance on 4A emergency diesel generator
- May 6, risk management for High aggregate risk due to extended out of service time for 4A emergency diesel generator
- May 17, risk management during maintenance on the Unit 3 startup transformer
- June 8, risk assessment and management after 3B emergency diesel generator was removed from service due to a failed fuel oil transfer pump (CR 2010-14915)
- June 30, risk management for Train 2 AFW when Train 1 AFW was declared inoperable for nitrogen backup line leak repair
b. Findings
No findings were identified.
==1R15 Operability Evaluations
a. Inspection Scope
==
For the five operability evaluations described in the condition reports (CR) listed below, the inspectors evaluated the technical adequacy of licensee evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred. The inspectors reviewed the final safety analysis report to verify that the system or component remained available to perform its intended function. In addition, when applicable, the inspectors reviewed compensatory measures implemented to verify that the plant design basis was being maintained. The inspectors also reviewed a sampling of condition reports to verify that the licensee was identifying and correcting any deficiencies associated with operability evaluations.
- CR 2010-9904, Standby Steam Generator Feed Pump B trouble alarm locked in without reflash due to alarm circuit issues
- CR 2010-8936, Lube oil leak identified during 4A EDG 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run from main oil pump
- CR 2010-6908 and 2007-38576 regarding 4A EDG turbo oil pump oil leak
- CR 2010-7918, operability of Unit 4 high head safety injection following identification of a void at point P-29 in the discharge piping. The review included structural evaluation in Numerical Applications Inc. Report NAI-1507-001, Evaluation of As-found Gas in Turkey Point Unit 4 Location P-29, and FPL Engineering Technical Response Memorandum, EDI-ENG-027, Attachment 2, Acceptance of safety injection supports for transient loads, dated 4-13-2010.
- CR 2010-10137, 3B Component Cooling Water Pump outboard mechanical seal leak
b. Findings
No findings were identified.
==1R17 Evaluations of Changes, Tests, or Experiments and Permanent Plant Modifications
a.
==
Inspection Scope
The inspectors reviewed selected samples of evaluations to confirm that the licensee had appropriately considered the conditions under which changes to the facility, Updated Final Safety Analysis Report (UFSAR), or procedures may be made, and tests conducted, without prior NRC approval. The inspectors reviewed evaluations for eight changes and additional information, such as drawings, calculations, supporting analyses, the UFSAR, and Technical Specifications (TS) to confirm that the licensee had appropriately concluded that the changes could be accomplished without obtaining a license amendment. The eight evaluations reviewed are listed in the List of Documents Reviewed.
The inspectors reviewed samples of changes for which the licensee had determined that evaluations were not required, to confirm that the licensees conclusions to screen out these changes were correct and consistent with 10CFR50.59. The fourteen screened out changes reviewed are listed in the List of Documents Reviewed.
The inspectors evaluated engineering design change packages for twelve material, component, and design based modifications to evaluate the modifications for adverse effects on system availability, reliability, and functional capability. The twelve modifications reviewed are as follows:
- PCM 08-025, Steam Dump to Atmosphere
- PCM 09-023, RPS Undervoltage Time Delay
- PCM 07-081, Containment Spray Pump Seal Modification
- PCM 08-012, Containment Spray Pump Material Changes
- PCM 07-087, 4B Diesel Oil Storage Tank Sample Valve Addition
- MSP 08-151, Unit 3 Emergency Diesel Generator Day Tank Level
- PCN 07-087, 4B DOST Sample Valve ADDN
Documents reviewed included procedures, engineering calculations, modification design and implementation packages, work orders, site drawings, corrective action documents, applicable sections of the living UFSAR, supporting analyses, TS, and design basis information. The inspectors additionally reviewed test documentation to ensure adequacy in scope and conclusion. The inspectors review was also intended to verify that all details were incorporated in licensing and design basis documents and associated plant procedures.
The inspectors also reviewed selected condition reports and the licensees recent self-assessment associated with modifications and screening/evaluation issues to confirm that problems were identified at an appropriate threshold, were entered into the corrective action process, and appropriate corrective actions had been initiated and tracked to completion.
b. Findings
No findings were identified.
==1R18 Plant Modifications
a. Inspection Scope
==
The inspectors reviewed the two temporary system modifications and one permanent plant modification listed below to ensure that that the modifications did not adversely affect safety system availability or reliability. The inspectors reviewed plant modifications for systems that were ranked high in risk for departures from design basis and for inadvertent changes that could challenge the systems to fulfill their safety function. For the permanent modification, the inspectors reviewed the licensees 10 CFR 50.59 screening to assure that NRC approval was not required prior to installation of the modification. The inspectors specifically checked material compatibility of added components, seismic qualification, adverse containment effects, and structural integrity.
The inspectors conducted plant tours and discussed system status with engineering and operations personnel to check for the existence of modifications that had not been appropriately identified and evaluated.
- Temporary change 10-016 to 3-OP-023, Emergency Diesel Generator, to allow filling of the EDG air flasks from a nitrogen trailer during piping replacement
- Temporary air handling unit staged in auxiliary building hallway for cooling the containment spray pump room
- Permanent Modification PCM 08-030, Unit 4 Rod Position Indication System Replacement
b. Findings
No findings were identified.
==1R19 Post Maintenance Testing
a. Inspection Scope
==
For the five post maintenance tests listed below, the inspectors reviewed the test procedures and either witnessed the testing and/or reviewed test records to determine whether the scope of testing adequately verified that the work performed was correctly completed and demonstrated that the affected equipment was operable. The inspectors used licensee procedure 0-ADM-737, Post Maintenance Testing, in their assessments.
- Unit 4: Satisfactory leak check under work order 40007951, following repair of a lubricating oil leak on the 4A emergency diesel generator (4K4A) main pressure pump discharge line (CR 2010-11424)
- Unit 4: Compressor run and leak check following 4A emergency diesel generator electric air compressor monthly preventive maintenance, done in accordance with 4-PMM-022.16, under work order 39015247-02
- Common: Satisfactory testing of the control room emergency ventilation using 0-OSP-025.1, Control Room Emergency Ventilation System Operability Test following replacement of relays per Work Order 39012972-01. Both channels of actuation circuitry were verified tested by the inspectors.
- Unit 3: 3B Component Cooling Water Pump inboard and outboard bearing replacements and outboard mechanical seal replacements under WO: 40003304-01, 40003304-02, and 37003677-01
- Unit 3: 3A intake cooling water pump tested using 3-OSP-019.1, Intake Cooling Water Inservice Test, following pump replacement under work order 38019976-01.
b. Findings
No findings were identified.
==1R22 Surveillance Testing
a. Inspection Scope
==
The inspectors either reviewed or witnessed the following six surveillance tests to verify that the tests met the technical specification requirements, the UFSAR, and the licensees procedural requirements and demonstrated that the systems were operationally ready to perform their intended safety functions. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the positions/status required for the system to perform its safety function. Two inservice testings (IST) were validated using the licensees Inservice Testing Program Fourth Ten Year Interval, dated March 11, 2004.
The inspectors verified that surveillance issues were documented in the corrective action program.
- 4-OSP-023.2, Unit 4A Diesel Generator 24 Hour Full Load Test
- 3-OSP-047.1, Unit 3B Charging Pump Inservice Test (IST)
- 0-OSP-074.3, Standby Steam Generator Feedwater Pumps Availability Test, Section 7.2, Operation of standby steam generator feedwater pump B in recirculation
- 3-OSP-206.2, Unit 3, Quarterly Inservice Valve Testing, Section 7.4.19 and 7.4.20 Stroke test of pressurizer power operated relief valve, block valves, MOV-3-535 and 536 (IST)
- 3-OSP-206.2, Quarterly Inservice Valve Testing, section 7.10, Residual Heat Removal, pump A suction isolation valve 3-752A (IST)
- 4-OSP-075.7, Auxiliary Feedwater Train 2 Backup Nitrogen Test
b. Findings
No findings were identified.
Cornerstone: Emergency Preparedness
1EP6 Drill Evaluation
.1 Simulator Based Training Evolution
a. Inspection Scope
On June 10, 2010, the inspectors observed an operating crew in the plant simulator and technical support center (TSC) staff during the second quarter emergency plan drill of the site emergency response organization. The drill included a loss of plant annunciators and declaration of an Unusual Event. Subsequently, a ground was simulated on the 3B 4160 volt safety bus resulting in loss of the bus with an accompanying reactor trip. A fire in the auxiliary transformer resulted in an alert declaration. The inspectors verified proper staffing of the emergency response facilities.
Later, an unisolable steam leak was simulated on the A main steam line followed by a steam generator tube rupture. The inspectors observed the Site Area Emergency declaration due to the loss of two of the fission product barriers. During the drill, the inspectors assessed operator actions to verify that emergency classification, notification, and protective action recommendations were made in accordance with the emergency plan implementing procedures and 10 CFR 50.72 requirements. The inspectors reviewed the event classifications and notifications to ensure these were made in accordance with licensee procedure, 0-EPIP-20101, Attachments 1 and 2, Turkey Point Classification Tables. The inspectors also observed whether the initial activation of the emergency response centers was timely and as specified in the licensees emergency plan. Technical Specifications required actions during the drill were reviewed to assess correct implementation. Drill critique items were discussed with the licensee and reviewed to verify that drill issues were identified and captured in the licensees corrective action program.
b. Findings
No findings were identified.
RADIATION SAFETY
2RS8 Radioactive Solid Waste Processing and Radioactive Material Handling, Storage, and
Transportation
a. Inspection Scope
The inspectors reviewed a licensee evaluation of radionuclide concentrations in resin and filter waste streams and the effect of using 10 CFR Part 61 analyses derived from resin samples to characterize shipments of radioactive filters. These evaluations were performed and reviewed in response to Unresolved Item (URI) 2009005-02. This URI is now closed.
b. Findings
Introduction:
The inspectors identified a Green non-cited violation (NCV) of 10 CFR Part 20.1501(a) for the failure to perform adequate surveys to meet the requirements of 10 CFR Part 20 Appendix G which states that shippers of radioactive waste must identify and quantify radionuclides contained in each waste container. Specifically, the inspectors determined that the use of resin samples to characterize shipments of mechanical filters was inadequate to ensure proper identification and quantification of the radionuclides present in each container.
Description:
During a review of the records package for radioactive waste shipment number 2009-063, the inspectors noted that the filters in the shipment had been characterized using a 10 CFR Part 61 analysis labeled 06 filter blend. Further inspection determined that the samples used to create 06 filter blend were actually samples of spent resin, rather than representative samples of the filters themselves.
This is contrary to the guidance in NRCs Branch Technical Position (BTP) on Waste Classification (1983) and Information Notice 86-20, Low-Level Radioactive Waste Scaling Factors, 10 CFR Part 61. These documents describe resin and filters as separate waste streams that require independent, representative, sampling of each.
This is due to the different properties of ion exchange resins and mechanical filters which tend to collect radioactive contaminants in differing concentrations. A subsequent analysis performed by the licensee confirmed that significant differences existed between 06 filter blend and a newly created filter waste stream composed of milipore filter samples of reactor coolant system water and spent fuel pool water. The BTP allows the use of indirect methods (e.g. scaling factors or gross radioactivity measurements) to classify waste with the caveat that the results be accurate to within a factor of 10. Of the 30 radionuclides detected in both 06 filter blend and the new milipore filter samples, 10 of these had scaling factor differences exceeding a factor of 10. An additional 10 radionuclides could not be compared since they were detected in one waste stream and not the other. The results indicate that 06 filter blend was not representative of the mechanical filter waste stream. An analysis was also performed to evaluate whether any of the three affected filter shipments (2008-001, 2008-003, and 2009-063) had been mis-classified per 10 CFR Part 61 (criteria for burial) or 10 CFR Part 71 (compliance with Department of Transportation regulations). The analysis results were reviewed by the inspectors and by a licensee-contracted vendor. It was determined that the three shipments were correctly classified and shipped, however shipment 2008-001 required additional filter averaging to comply with 10 CFR Part 61 Class C limits. The inspectors also noted that although the waste classification remained the same in all three cases, the specific radionuclides that contributed the most to waste classification were different, i.e., filters characterized using 06 filter blend were Class C based mostly on Ni-63 concentration whereas filters classified using the new filter waste stream were Class C based on transuranic concentration. Therefore, the radionuclide distributions for the containers listed on NRC Form 541 Uniform Low-Level Radioactive Waste Manifest for shipments 2008-001, 2008-003, and 2009-063 were not accurate.
Analysis:
The inspectors determined that the failure to use representative samples, per BTP guidance, to characterize radioactive waste shipments was a performance deficiency and was reasonably within the licensee=s ability to foresee and correct. The finding is more than minor because it is associated with the Public Radiation Safety cornerstone attribute of Programs and Processes and adversely affects the cornerstone objective of ensuring adequate protection of public health and safety from exposure to radioactive materials released into the public domain as a result of routine civilian nuclear reactor operation. Analyses performed to characterize shipments of radioactive waste must be accurate in order to ensure compliance with burial criteria and to ensure first-responders (in the event of an accident) and the general public remain safe while the packages are in-transit. The finding was assessed using the Public Radiation Safety Significance Determination Process (SDP). Based on the fact that none of the filter waste was under-classified, the finding was determined to be of very low safety significance (Green). The inspectors noted that the licensee made changes to how the filter waste stream is sampled as part of their corrective actions. This finding has a crosscutting aspect of Human Performance, Decision Making H.1(b), because the decision to use resin samples to characterize mechanical filter shipments was based on incorrect assumptions, i.e., that spent resin samples would be representative of the filter waste stream, and those assumptions were not demonstrated to be conservative prior to implementation.
Enforcement:
10 CFR Part 20.1501(a) states, in part, AEach licensee shall make or cause to be made, surveys that -
- (1) May be necessary for the licensee to comply with the regulations in this part. 10 CFR Part 20, Appendix G (I)(C) states, in part, The shipper of radioactive waste shall provide the following information on the uniform manifest regarding the waste and each disposal container of waste in the shipment:
- (10) The identities and activities of individual radionuclides contained in each container.
Contrary to this, three shipments of radioactive filters (2008-001, 2008-003, and 2009-063) were sent for waste processing without the licensee having performed adequate surveys to determine the identities and quantities of individual radionuclides contained in each container. Because this violation was of very low safety significance and was entered into the licensee=s corrective action program (CR 2009-32955), this violation is being treated as an NCV, consistent with the Enforcement Policy: NCV 05000250, 251/2010003-01: Failure to perform adequate surveys to ensure proper estimation of radionuclide concentrations in mechanical filter waste shipments.
OTHER ACTIVITIES
4OA2 Problem Identification and Resolution
.1 Daily Review
a. Inspection Scope
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensees corrective action program. This review was accomplished by reviewing daily summaries of condition reports and by reviewing the licensees electronic condition report database. Additionally, a reactor coolant system unidentified leakage was checked on a daily basis to verify no substantive or unexplained changes.
b. Findings
No findings were identified.
.2 Annual Sample Review
a. Inspection Scope
The inspectors selected the following two condition reports for detailed review and discussion with the licensee. The condition reports were reviewed to ensure that an appropriate evaluation was performed and appropriate corrective actions were specified and prioritized. Other attributes checked included disposition of operability and resolution of the problem including cause determination and corrective actions. The inspectors evaluated the condition reports in accordance with the requirements of the licensees corrective actions process as specified in licensee procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action. The inspectors reviewed the cumulative effects of the operator workarounds that were in place to verify that those effects could not increase an initiating event frequency, affect multiple mitigating systems, or affect the ability of operators to properly respond to plant transients and accidents. The inspectors also reviewed operator workarounds to verify that the licensee was identifying operator workaround problems at an appropriate threshold and entering them in the corrective action program.
- CR 2010-13740: During normal start of 4A emergency diesel generator, the low fuel oil pressure alarm annunciated
b. Findings
No findings were identified.
.3 Semi-Annual Trend Review
a. Inspection Scope
As required by Inspection Procedure 71152, Identification and Resolution of Problems, the inspectors reviewed the licensees corrective action program and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector corrective actions item screening discussed in section 4OA2.1 above, plant status reviews, plant tours, document reviews, and licensee trending efforts. Among the documents reviewed was the Turkey Point Station Performance Improvement Health Report, 1st Quarter 2010, dated May 14, 2010. The inspectors review nominally considered the six month period of January through June 2010. Corrective actions associated with a sample of the issues identified in the licensees corrective action program were reviewed for adequacy.
b.
Assessment and Observations
No findings were identified..
4OA3 Follow-up of Events
a. Inspection Scope
The inspectors reviewed the licensees personnel performance during an unplanned trip of the Unit 3 B condensate pump resulting in power reduction on June 3, 2010.
b. Findings
Introduction:
(Green) A Self-Revealing Non-cited Violation of Technical Specification requirements was identified when rod position indication for two rod control cluster assemblies (RCCs) drifted out of tolerance with the associated rod group position indication. Contrary to technical specification requirements, rod positions were neither re-aligned with the group counter nor was reactor power reduced to less than 90 percent within the specified one hour action time.
Description:
On June 3, 2010, the 3B condensate pump tripped causing a small perturbation that resulted in reactor power being reduced to 97 percent. Afterwards, at 2045 hours0.0237 days <br />0.568 hours <br />0.00338 weeks <br />7.781225e-4 months <br />, the rod position indication for RCCs M8 and H4 drifted to 219 steps with the Group D demand at 206 (a misalignment of 13 steps). Technical Specification 3.1.3.1 allows a rod misalignment of 12 steps when reactor power is greater than 90 percent.
The Action statement requires that within one hour, (before 2145 hours0.0248 days <br />0.596 hours <br />0.00355 weeks <br />8.161725e-4 months <br />) alignment be restored to within the allowed 12 steps or reduce reactor power to less than 90 percent.
There is also a third option to place the plant in hot standby within the next six hours if RCC alignment cannot be attained.
When the misalignment was noted, the operators entered off-normal procedures for misaligned control rods and attempted to obtain a flux map that would verify actual rod position. Because of problems with the flux mapper, the Unit Supervisor (instead of the Shift Technical Advisor) attempted to complete the flux mapping. In the first flux map attempt, an unsatisfactory trace was obtained and the Shift Manager directed a second attempt. The second attempt failed due to paper jam. At 2138 hours0.0247 days <br />0.594 hours <br />0.00354 weeks <br />8.13509e-4 months <br />, the Shift Manager directed the Shift Technical Advisor (licensed) to reduce reactor power to less than 90 percent to comply with Technical Specification requirements. The down power was briefed and then completed at 2205 hours0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.390025e-4 months <br />. During this time, the Unit Supervisor attempted to obtain a satisfactory flux map. The licensee documented the informal switching or roles between the shift technical advisor and the unit supervisor in CR 2010-16169.
Analysis:
Failure to properly implement technical specification requirements for rod position misalignment and either restore proper alignment or reduce reactor power within the required action time was a performance deficiency. The finding was more than minor because if inaccurate rod position indication is left uncorrected, there is an increased potential for an actual rod misalignment being uncorrected affecting accident analysis assumptions. The Initiating Events cornerstone was affected because rod position alignment assures that accident analysis assumptions affecting power distribution and shutdown margin are maintained. The inspectors evaluated the finding using NRC Inspection Manual 0609, Attachment 0609.04, Initial Screening and Characterization of Findings (because the finding had not been screened) and classified the finding to be of very low safety significance (Green) using the Transient Initiator tool.
The cross-cutting aspect of Human Performance, Decision Making (H.1.a) was affected when supervisory personnel did not implement their roles and authorities to assure safety by implementing Technical Specification requirements within allowed time limits.
Enforcement:
Technical Specification 3.1.3.1.b requires that with more than one full length rod misaligned from the group step counter by more than 12 steps and THERMAL POWER greater than 90 percent of rated thermal power, within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, reduce thermal power to less than 90 percent and confirm that all indicated rod positions are within the allowed rod misalignment (18 steps). Contrary to the above, on June 3, 2010, with Unit 3 at 97 percent power at 2045 hours0.0237 days <br />0.568 hours <br />0.00338 weeks <br />7.781225e-4 months <br />, rod positions for RCCs M8 and H4 were misaligned from the group counter in excess of 12 steps and power was not reduced to less than 90 percent within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />. The occurrence was self-revealing to the operators who completed action to reduce power to less than 90 percent at 2205 hours0.0255 days <br />0.613 hours <br />0.00365 weeks <br />8.390025e-4 months <br /> (one hour and 20 minutes). The issue was documented in the corrective action program as CR 2010-14724. Because this issue is of very low safety significance and has been entered into the licensees corrective action program, the violation is being treated as a Non-cited Violation consistent with Section VI.A.1 of the NRC Enforcement Policy: NCV 05000250, 251/2010-03-02, Failure to Implement TS Requirements Regarding Rod Position Indication.
4OA6 Exit
Exit Meeting Summary
The resident inspectors presented the inspection results to Mr. Kiley and other members of licensee management on July 19, 2010. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information.
ATTACHMENT: SUPPPLEMENTAL INFORMATION
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
Licensee personnel
- N. Bach, Chemistry Manager
- C. Cashwell, Radiation Protection Manager
- R. Coffey, Maintenance Manager
- M. Crosby, Quality Manager
- J. Garcia, Engineering Manager
- M. Epstein, Emergency Preparedness Manager (Acting)
- M. Kiley, Site Vice-President
- J. Patterson, Fire Protection Supervisor
- P. Rubin, Plant General Manager
- R. Tomonto, Licensing Manager
- S. Shafer, Assistant Operations Manager
- R. Wright, Operations Manager
NRC personnel
- L. Wert, Director, Division of Reactor Projects
- M. Sykes, Chief, Reactor Projects Branch 3
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED
Closed
- 05000250, 251/2009-05-02
URI Inappropriate characterization of RCS filters for transportation and disposal (Section 2RS8)
Opened and Closed
- 05000250, 251/2010-03-01 NCV Failure to perform adequate surveys to ensure proper estimation of radionuclide concentrations in mechanical filter waste shipments (Section 2RS8)
- 05000250, 251/2010-03-02 NCV Failure to implement TS requirements regarding
rod position indication (Section 4OA3)
LIST OF DOCUMENTS
/DATA REVIEWED