IR 05000346/2011008: Difference between revisions
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{{#Wiki_filter: | {{#Wiki_filter:April 19, 2011 | ||
== | ==SUBJECT:== | ||
DAVIS-BESSE NUCLEAR POWER STATION - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION 05000346/2011008 | |||
==Dear Mr. Allen:== | ==Dear Mr. Allen:== | ||
On March 17, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution (PI&R) team inspection at your Davis-Besse Nuclear Power Station. The enclosed report documents the inspection findings, which were discussed on March 17, 2011, with Mr. Brian Boles and other members of your staff. | |||
This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, and compliance with the | This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, and compliance with the Commissions rules and regulations and the conditions of your operating license. Within these areas, the inspection involved examination of selected procedures and representative records, observations of activities, and interviews with personnel. | ||
The inspection team concluded that on the basis of the sample selected for review, in general, problems were properly identified, evaluated, and corrected. The team noted that the station staff reviewed operating experience for applicability to station activities. Audits and self-assessments were performed at an appropriate level to identify most deficiencies. Based on the independent assessment of safety culture results, interviews conducted during the inspection, and review of the employee concerns program, freedom to raise nuclear safety concerns was demonstrated. | The inspection team concluded that on the basis of the sample selected for review, in general, problems were properly identified, evaluated, and corrected. The team noted that the station staff reviewed operating experience for applicability to station activities. Audits and self-assessments were performed at an appropriate level to identify most deficiencies. Based on the independent assessment of safety culture results, interviews conducted during the inspection, and review of the employee concerns program, freedom to raise nuclear safety concerns was demonstrated. | ||
Based on the results of this inspection, no findings were identified. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room) | Based on the results of this inspection, no findings were identified. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS) | ||
. | component of NRC's document system (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room). | ||
Sincerely, | Sincerely, | ||
/RA/ | /RA/ | ||
Cameron, Chief Branch 6 Division of Reactor Projects | Jamnes L. Cameron, Chief Branch 6 Division of Reactor Projects | ||
Docket No. 50-346 License No. NPF-3 | Docket No. 50-346 License No. NPF-3 | ||
===Enclosure:=== | ===Enclosure:=== | ||
Inspection Report | Inspection Report 05000346/2011008 w/Attachment: Supplemental Information | ||
REGION III== | REGION III== | ||
| Line 48: | Line 47: | ||
50-346 License No: | 50-346 License No: | ||
NPF-3 Report No: | NPF-3 Report No: | ||
05000346/2011008 Licensee: | |||
Facility: Davis-Besse Nuclear Power Station Location: Oak Harbor, OH Dates: February 14, | FirstEnergy Nuclear Operating Company (FENOC) | ||
A. Garmoe, Project Engineer, Team Lead J. Rutkowski , Senior Resident Inspector , Davis-Besse, Team Lead J. Bozga , Reactor Inspector, Mechanical C. Brown, Reactor Inspector, Electrical A. Wilson , Resident Inspector Approved by: | Facility: | ||
Jamnes L. Cameron | Davis-Besse Nuclear Power Station Location: | ||
, Chief Branch 6 Division of Reactor Projects Enclosure | Oak Harbor, OH Dates: | ||
February 14, 2011, through March 17, 2011 Inspectors: | |||
A. Garmoe, Project Engineer, Team Lead | |||
J. Rutkowski, Senior Resident Inspector, | |||
Davis-Besse, Team Lead | |||
J. Bozga, Reactor Inspector, Mechanical | |||
C. Brown, Reactor Inspector, Electrical | |||
A. Wilson, Resident Inspector | |||
Approved by: | |||
Jamnes L. Cameron, Chief Branch 6 Division of Reactor Projects | |||
Enclosure | |||
=SUMMARY OF FINDINGS= | =SUMMARY OF FINDINGS= | ||
IR | IR 05000346/2011008; 02/14/2011 - 03/17/2011; Davis-Besse Nuclear Power Station; Routine | ||
Biennial Problem Identification and Resolution (PI&R) Inspection This inspection was performed by three NRC regional inspectors, one Davis-Besse Nuclear Power Station senior resident inspector, and the Davis-Besse Nuclear Power Station resident inspector. No findings or violations of NRC requirements were identified during this inspection. | |||
The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006. | |||
-1649, | |||
On the basis of the sample selected for review, the team concluded that implementation of the corrective action program (CAP) at Davis-Besse Nuclear Power Station was generally effective | On the basis of the sample selected for review, the team concluded that implementation of the corrective action program (CAP) at Davis-Besse Nuclear Power Station was generally effective. | ||
On the basis of interviews conducted during the inspection, workers at the site expressed freedom to enter safety concerns into the CAP. | The licensee had a low threshold for identifying problems and entering them in the CAP. Items entered into the CAP were screened and prioritized in a timely manner using established criteria; were properly evaluated commensurate with their safety significance; and corrective actions were generally implemented in a timely manner, commensurate with the safety significance. The team noted that the licensee reviewed operating experience for applicability to station activities. Audits and self-assessments were determined to be performed at an appropriate level to identify most deficiencies. On the basis of interviews conducted during the inspection, workers at the site expressed freedom to enter safety concerns into the CAP. | ||
Problem Identification and Resolution A | Problem Identification and Resolution A. | ||
No findings were identified. | |||
=== | ===NRC-Identified=== | ||
and Self-Revealed Findings B. | |||
No violations of significance were identified. | |||
===Licensee-Identified Violations=== | |||
=REPORT DETAILS= | =REPORT DETAILS= | ||
==OTHER ACTIVITIES== | ==OTHER ACTIVITIES== | ||
{{a|4OA2}} | {{a|4OA2}} | ||
== | ==4OA2 Problem Identification and Resolution== | ||
The activities documented in Sections | |||
===.1 through.4 constituted one biennial sample of=== | |||
problem identification and resolution as defined in Inspection Procedure 71152. | |||
(71152B) | |||
===.1 a.=== | |||
Assessment of the Corrective Action Program Effectiveness The inspectors reviewed the licensees Corrective Action (CA) program implementing procedures and attended CA program meetings to assess the implementation of the CA program by site personnel. | |||
The inspectors | Inspection Scope The inspectors reviewed risk and safety significant issues in the licensees CA program since the last NRC Problem Identification and Resolution (PI&R) inspection in April 2009. The selection of issues ensured an adequate review of issues across NRC cornerstones. The inspectors used issues identified through NRC generic communications, department self assessment, licensee audits, operating experience reports, and NRC documented findings as sources to select issues. Additionally, the inspectors reviewed Condition Reports (CRs) generated as a result of facility personnels performance in daily plant activities. In addition, the inspectors reviewed CRs and a selection of completed investigations from the licensees various investigation methods, which included root cause, full apparent cause, limited apparent cause, and common cause investigations. | ||
The inspectors | The inspectors selected the control rod drive system to review in detail. The inspectors review was to determine whether the licensee staff were properly monitoring and evaluating the performance of these systems through effective implementation of station monitoring programs. A 5 year review on the control rod drive system was undertaken to assess the licensees efforts in monitoring for system degradation due to aging aspects. The inspectors also performed partial system walkdowns of the auxiliary feedwater system and decay heat system. A review of the use of the station maintenance rule program to help identify equipment issues was also conducted. | ||
During the reviews, the inspectors determined whether the licensee staffs actions were in compliance with the facilitys corrective action program and 10 CFR Part 50, Appendix B requirements. Specifically, the inspectors determined whether licensee personnel were identifying plant issues at the proper threshold, entering the plant issues into the stations CA program in a timely manner, and assigning the appropriate prioritization for resolution of the issues. The inspectors also determined whether the licensee staff assigned the appropriate investigation method to ensure the proper determination of root, apparent, and contributing causes. The inspectors also evaluated the timeliness and effectiveness of corrective actions for selected issue reports, completed investigations, and NRC findings, including non-cited violations. | |||
-cited violations. | |||
b. | b. | ||
| Line 103: | Line 117: | ||
In addition, the inspectors noted that the licensee trends equipment and human performance on a regular basis. | In addition, the inspectors noted that the licensee trends equipment and human performance on a regular basis. | ||
Effectiveness of Problem Identification The inspectors identified one example of a weakness with regard to entering conditions into the corrective action program at a low threshold. The licensee initiated CR 11-89925 after I&C technicians inadvertently tripped the radwaste ventilation system while performing a surveillance to calibrate radwaste area exhaust process radiation monitor RE5405A. The licensee | Effectiveness of Problem Identification The inspectors identified one example of a weakness with regard to entering conditions into the corrective action program at a low threshold. The licensee initiated CR 11-89925 after I&C technicians inadvertently tripped the radwaste ventilation system while performing a surveillance to calibrate radwaste area exhaust process radiation monitor RE5405A. The licensee has been changing out radiation monitors from analog to digital, thus two active procedures were in place to perform the calibration. Prior to calibrating radiation monitor RE5405A, a digital radiation monitor, the technicians were incorrectly provided with the procedure used for calibrating an analog radiation monitor. | ||
The analog procedure performs steps in a slightly different order than the digital procedure, which caused the radwaste ventilation system to trip offline. One of the technicians involved had caught the mistake of being given the wrong procedure on several previous occasions, but did not catch the error in this instance. This event could have been prevented had a condition report been written for the previous instances of being given the wrong procedure. | |||
Observations | |||
No findings were identified. | |||
Findings | Findings | ||
: (2) The inspectors reviewed the classification of CRs for resolution and determined that, in general, CRs were assigned appropriate prioritization and evaluation levels and evaluations in apparent cause and root cause reports that were reviewed were adequate. Effectiveness of Prioritization and Evaluation of Issues The inspectors reviewed CR 10 | : (2) The inspectors reviewed the classification of CRs for resolution and determined that, in general, CRs were assigned appropriate prioritization and evaluation levels and evaluations in apparent cause and root cause reports that were reviewed were adequate. | ||
-75350, | |||
Effectiveness of Prioritization and Evaluation of Issues | |||
The inspectors reviewed CR 10-75350, Turbine Building HELB Concerns in CCW Pump Room. The inspectors noted that the immediate operability determination was based on engineering judgment that was not numerically or analytically based. Upon further discussion with the Engineering Department, the operability determination was updated to include numerically and analytically based information. The inspectors concluded that the Shift Manager accepted engineering judgment as a basis for operability and did not sufficiently challenge the information provided by Engineering to ensure an adequate basis for operability was provided. | |||
Observations The inspectors also reviewed CR 10 | Observations The inspectors also reviewed CR 10-87473, Pipe Stress Calculations for Temporary Shielding. Pipe stress analysis and pipe support calculations were verified to be in conformance with design and licensing basis requirements for decay heat piping systems. However, the inspectors did identify three design control violations of minor significance involving the placement of lead shielding on piping systems. The minor violations were entered into the CA program as CR 11-90280, CR 11-90326, and CR 11-90347. | ||
-87473, | |||
-90326, and CR 11-90347. No findings were identified. | No findings were identified. | ||
Findings | Findings | ||
: (3) In general, the inspectors noted that the corrective actions addressed the cause of the identified problem, and appeared to have been effective in the majority of samples reviewed. The inspectors noted that at least in one department there were some inconsistencies in closing out corrective actions and that those closeouts were not in accordance with station expectations. | : (3) In general, the inspectors noted that the corrective actions addressed the cause of the identified problem, and appeared to have been effective in the majority of samples reviewed. The inspectors noted that at least in one department there were some inconsistencies in closing out corrective actions and that those closeouts were not in accordance with station expectations. | ||
Effectiveness of Corrective Actions The inspectors identified several examples where licensee personnel appeared to demonstrate a lack of rigor in complying with stated requirements of the CA program | Effectiveness of Corrective Actions The inspectors identified several examples where licensee personnel appeared to demonstrate a lack of rigor in complying with stated requirements of the CA program. | ||
Observations Procedure NOP-LP-2001, Corrective Action Program, Section 4.17, states that all approved CAs shall be tracked in the condition report database from initiation until implementation. Additionally, a licensee-generated memorandum sent to Davis-Besse managers on March 10, 2010, re-iterated that CAs identifying that something will be done should not be closed until the action is done. The inspectors reviewed CR 09-55141, Chemistry Plant Status Control Standing Order Noncompliance, and observed that CA #9 was closed on August 26, 2009, with work order system notifications to track remaining open items. Two of the notifications (600566034 and 600566035) were still open as of February 17, 2011. Licensee personnel stated that the CAs were completed but the notifications had not been updated in a timely manner. Additionally, it was identified that CAs #5 and #9 had not been accomplished as written, even though the CAs were closed in the CA program electronic database. As a result of the inspectors observations, the licensee initiated CR 11-89901 and CR 11-89748. | |||
, | |||
, | |||
The inspectors reviewed CR 09-67079, Weaknesses in the Boron-10 Correction Factor Program, which was written in response to licensee identified ineffective and incomplete CA from CR 06-06669, Boron 10 Isotopic Composition Not Accounted for in BWST, BAATS, CFTS. Corrective action #3 of CR 09-67079 called for a full review of all Chemistry full and limited apparent causes, dating to 2006, to ensure that all CAs generated as a result of those evaluations were tracked to completion. The results of that review were documented in CR 10-72273, Incomplete Documentation of Corrective Actions, which included several examples of documentation issues or closure issues. | |||
manager withdrew the document until there was a revised analysis of condition applicability to similar circumstances. As of February 15, 2011, the CR had not been reviewed by the CARB, which is inconsistent with the CARB review time frame requirements of NOP | The inspectors noted that the review did not identify that CA #9 from CR 09-55141 had remaining open items. | ||
-LP-2001, | |||
-89733 to document this issue. The inspectors reviewed CR 09 | It was also determined that CA #4 of CR 09-67079 was closed on April 27, 2010, to an action plan that listed actions to be tracked using work order notifications 600612198, 600612199, and 600612200. The action plan stated that the due date for completion of the actions was November 1, 2010. As of February 16, 2011, those notifications were still open even though the licensee stated that the actions had been completed. The licensee documented this issue in CR 11-89741. | ||
-63254, | |||
-C-09-08-22: | The inspectors reviewed CR 10-73290, Unattended Vehicle in the 75 Foot Exclusion Zone near the Dry Fuel Storage Pad, which was written on March 12, 2010, to document a finding issued by the NRC. All CAs and the limited apparent cause analysis were documented as completed as of April 9, 2010. The CR was scheduled to be reviewed by the Corrective Action Review Board (CARB) on November 1, 2010. | ||
-cited violations from the NRC and performed numerous apparent cause evaluations. The inspectors view the lack of a CA to address the most recent identified cause, particularly when considered as part of a long | |||
-standing issue, as a weakness in the ability to promptly take effective corrective actions. | However, the sponsoring manager withdrew the document until there was a revised analysis of condition applicability to similar circumstances. As of February 15, 2011, the CR had not been reviewed by the CARB, which is inconsistent with the CARB review time frame requirements of NOP-LP-2001, Corrective Action Program. The licensee initiated CR 11-89733 to document this issue. | ||
The inspectors reviewed CR 09-63254, Finding MS-C-09-08-22: Ineffective Corrective Action Implementation for HSM. The CR discussed a CA from a full apparent cause evaluation (ACE) that had not been effectively implemented. The licensee performed a limited ACE to determine why the CA from the full ACE had not been effectively implemented. The limited ACE identified the cause as a failure to fully follow the CR process; however the inspectors identified that no CA was assigned to address the cause. The inspectors noted that the underlying technical issue, combustible materials within 75 feet of the horizontal storage modules (dry cask spent fuel storage), is an issue that the licensee has not been able to effectively correct for several years. Dating back to 2006, the licensee received two non-cited violations from the NRC and performed numerous apparent cause evaluations. The inspectors view the lack of a CA to address the most recent identified cause, particularly when considered as part of a long-standing issue, as a weakness in the ability to promptly take effective corrective actions. | |||
No findings were identified. | No findings were identified. | ||
| Line 151: | Line 159: | ||
Findings | Findings | ||
===.2 a. Assessment of the Use of Operating Experience | ===.2 a.=== | ||
Assessment of the Use of Operating Experience The inspectors reviewed the licensees implementation of the facilitys Operating Experience (OE) program. Specifically, the inspectors reviewed implementing operating experience program procedures, completed evaluations of OE issues and events, monthly assessments of the OE composite performance indicators, and attended CA program meetings to observe the use of OE information. The inspectors review was to determine whether the licensee was effectively integrating OE experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel, whether the licensees program was sufficient to prevent future occurrences of previous industry events, and whether the licensee effectively used the information in developing departmental assessments and facility audits. The inspectors also assessed whether corrective actions, as a result of OE experience, were identified and effectively and timely implemented. | |||
Inspection Scope b. | |||
The inspectors | The inspectors determined that the overall performance of the operating experience program was adequate. | ||
Assessment | |||
The inspectors reviewed the licensees dispositioning of Information Notice (IN) 2008-02, Findings Identified During Component Design Basis Inspections (CDBI), which communicated issues identified during recent CDBI inspections. The inspectors noted that the licensees review of IN 2008-02 was closed to existing procedures and practices, such as the OE Program, Latent Issues Review Process, and the Engineering Design Process. There was very little, if any, applicability review performed by the licensee. | |||
-02, | |||
Observations | |||
No findings were identified. | |||
Findings | Findings | ||
===.3 a. | ===.3 a.=== | ||
Assessment of Self-Assessments and Audits The inspectors assessed the licensee staffs ability to identify and enter issues into the CA program, prioritize and evaluate issues, and implement effective CAs, through efforts from departmental assessments and audits. | |||
-Assessments and Audits The inspectors assessed the licensee | |||
Inspection Scope b | Inspection Scope b. | ||
The inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying most issues and enhancement opportunities at an appropriate threshold level. However, the inspectors noted at least one assessment that did not identify issues subsequently identified by the NRC. The inspectors concluded that these audits and self-assessments were completed by personnel knowledgeable in the subject area. In many cases, these self-assessments and audits had identified issues that were not previously recognized by the station. | |||
- | |||
- | |||
The self-assessment was prepared in August 2010, prior to the NRC 95001 supplemental inspection that was conducted in September 2010. The supplemental inspection was conducted in response to a finding of low to moderate (White)safety significance identified in 2009 for the failure to recognize an event in the electrical switchyard that met the emergency action level conditions for declaring an Alert. Self | Assessment Observations The inspectors reviewed licensee self-assessment SN-SA-255, Pre-NRC IP 95001 Inspection Assessment (Davis-Besse EP), for adequacy. The self-assessment was prepared in August 2010, prior to the NRC 95001 supplemental inspection that was conducted in September 2010. The supplemental inspection was conducted in response to a finding of low to moderate (White) safety significance identified in 2009 for the failure to recognize an event in the electrical switchyard that met the emergency action level conditions for declaring an Alert. Self-assessment SN-SA-255 states that the assessment verified that actions taken have been largely effective in correcting the root and contributing causes of the failure to classify. However, the NRC 95001 inspection revealed weaknesses with the adequacy of the licensees extent of cause evaluation and concerns about whether the corrective actions would prevent recurrence. | ||
-assessment SN | |||
-SA-255 states that the assessment verified that | |||
Site Self Assessments The NRC kept the White finding open until the corrective actions and extent of cause evaluation were expanded. A follow-up NRC 95001 inspection reviewed the updated information and closed the White finding in December 2010. Based on the NRCs concerns during the initial 95001 inspection, the inspectors questioned the adequacy of self-assessment SN-SA-255. The inspectors identified weaknesses in the corrective actions and extent of cause reviews performed by the self-assessment. The licensee initiated CR 11-90395 in response to the inspectors observations. | |||
The NRC kept the White finding open until the corrective actions and extent of cause evaluation were expanded. A follow-up NRC 95001 inspection reviewed the updated information and closed the White finding in December 2010. Based on the | |||
-SA-255. The inspectors identified weaknesses in the corrective actions and extent of cause | |||
The inspectors also reviewed self | The inspectors also reviewed self-assessment IP-SA-11-113, Integrated Performance Assessment and Trending for Operations, Second 6 months of 2010. The inspectors identified that the self-assessment failed to identify a trend that was identified by NRC inspectors during the fourth quarter of 2010. Specifically, the NRC integrated fourth quarter Inspection Report 05000356/2010005 identified an adverse trend related to the licensees management of Technical Specifications and Limiting Conditions for Operations, with several examples identified during the third and fourth quarters of 2010. | ||
-assessment IP | |||
-SA-11-113, | |||
. | |||
-assessment failed to identify a trend that was identified by NRC inspectors during the fourth quarter of 2010. Specifically, the NRC integrated fourth quarter Inspection Report 05000356/2010005 identified an adverse trend related to the | |||
The | The inspectors noted a weakness in that self-assessments, including IP-SA-11-113, review NRC inspection reports for findings and violations, but do not review the semi-annual trend review section of the report. A review of the semi-annual trend section could have led the self-assessment to document a potential adverse trend in Operations that was relevant to the second half of 2010. | ||
- | |||
- | |||
-assessment. | |||
Self Assessment SN-SA-10-352, Work Order Package Completeness and Associated Impact on the Maintenance Shops, was also reviewed by the inspectors. The licensee conducted this assessment to review why 64 work orders had been placed in Additional Planning status between July 26 and October 4, 2010. | |||
The assessment conclusion did not identify any negative trends attributable to a particular department or process but included the statement, Work Planning needs to continue to strive for increased quality in the work orders. Procedure NOBP-LP-2001, FENOC Self-Assessment/Benchmarking, states that assessment results should be grouped as strengths, recommendations, and deficiencies. Deficiencies and recommendations are required by procedure to have corrective action or notification assignments. The statement referenced was not listed as a deficiency or recommendation and, therefore, had no associated corrective action or notification action that could communicate the insight to plant staff. Discussion with licensee personnel revealed that the need to strive for increased Work Order quality was being reinforced by a corrective action from the Root Cause Evaluation in CR 10-86565, which is not related to SN-SA-10-352. While the concern over work order quality in assessment SN-SA-10-352 was being addressed by a separate unrelated action, the inspectors concluded that, absent the unrelated Root Cause Evaluation, this meaningful observation would have likely not been communicated to plant staff. Such communication could have been accomplished through an assigned corrective action or notification from the self-assessment. | |||
The inspectors, | The inspectors reviewed assessments and audits conducted by Fleet Oversight, including the quarterly assessment report from the fourth quarter of 2010. Ratings of the performance of station organizations are assigned by Fleet Oversight in accordance with procedure NOBP-LP-2023, Nuclear Operating Business Practice, Performance Assessment. That procedure specifies four levels of effectiveness using a color scheme of green, white, yellow, and red. In the fourth quarter of 2010, all departments Fleet Oversight Assessments were rated as effective (White), with steady, improved, or improving trends. The inspectors noted several departments were rated as effective for all quarters in 2010. | ||
This included the Chemistry department which, in the fourth quarter of 2010, was rated as marginally effective (Yellow) in a separate assessment, MS-C-10-08-02, a multi-site audit of chemistry and environmental areas. That audit identified recurring significant issues in the laboratory quality control program, failure to satisfy Technical Specification requirements for changes to the Offsite Dose Control Manual, and issues related to chemistry sampling and analysis. The inspectors, while not having a general concern with the overall effectiveness of the assessment and audit program, did question the rating of effective for all station departments. | |||
- | |||
The assessments show the Site Protection department transitioning from | The inspectors also reviewed Fleet Oversight quarterly assessments for the Site Protection department for the fourth quarter 2009 and all four quarters of 2010, based on review of Condition Report 10-70483, Site Protection Rated Marginally Effective for Fourth Quarter 2009. The assessments show the Site Protection department transitioning from marginally effective (Yellow) to effective (White). The inspectors review of the assessments identified that, when taken as stand-alone documents, it was difficult to verify the conclusions that were reached. The main reason for this appears to be that the assessments focus on different items each quarter, thereby making it more difficult to trend performance. The inspectors did, ultimately, determine that the assessment conclusions were appropriate using information from other performance reports in addition to information included in the quarterly assessments. | ||
-alone documents, it was difficult to verify the conclusions that were reached. The main reason for this appears to be that the assessments focus on different items each quarter, thereby making it more difficult to trend performance. The inspectors did, ultimately, determine that the assessment conclusions were appropriate using information from other performance reports in addition to information included in the quarterly assessments. | |||
The inspectors noted that the licensee-provided listing of assessments did not indicate any assessment of the | The inspectors noted that the licensee-provided listing of assessments did not indicate any assessment of the licensees overall assessment program. The inspectors were advised that such an assessment was scheduled for the second quarter of 2011. | ||
No findings were identified. | No findings were identified. | ||
| Line 226: | Line 207: | ||
Findings | Findings | ||
===.4 a. Assessment of Safety Conscious Work Environment | ===.4 a.=== | ||
Assessment of Safety Conscious Work Environment The inspectors assessed the licensees safety-conscious work environment (SCWE)through the reviews of the facilitys employee concerns program (ECP) implementing procedures, discussions with the ECP coordinator, interviews with personnel from various departments, and reviews of issue reports. The inspectors also reviewed the results from a 2010 Safety Culture Survey. | |||
Inspection Scope The inspectors interviewed approximately 30 individuals from various departments to assess their willingness to raise nuclear safety issues. The individuals were selected to provide a distribution across the various departments at the site and included long-term contractors. The sample was of individuals predominantly at first-line supervision and below first-line supervision. In addition to assessing individuals willingness to raise nuclear safety issues, the interviews also addressed changes in the CA program and plant environment over the past 2 years. Other items discussed included: | |||
* knowledge and understanding of the CA program; | |||
* effectiveness and efficiency of the CA program; | |||
* willingness to use the CA program; | |||
* managements support of the CA program; | |||
* feedback on issues raised; and | |||
* ease of input to the CA database system. | |||
b. | |||
Interviews indicated that the licensee has an environment where people are free to raise issues without fear of retaliation. Documents provided to the inspectors regarding the 2010 safety culture assessment stated that Davis-Besse Nuclear Power Station maintained a healthy safety culture. Based on a review of the survey data, the inspectors concluded that the data supported that conclusion. | |||
Assessment All interviewees indicated that station personnel would raise safety issues and were comfortable doing so. All individuals knew that, in addition to the CA program, they could raise issues to their management, the ECP, or the NRC. None of the individuals interviewed indicated they had been retaliated against for raising issues nor were they aware of anyone who had been retaliated against. Several interviewees indicated that they believe writing a condition report will result in more work for them and others indicated that condition reports can be perceived negatively by individuals involved in the documented activity. However, all individuals indicated that they would nevertheless raise safety issues through condition reports. | |||
No findings were identified. | |||
Findings 4OA6 | |||
===.1 Management Meetings=== | |||
On March 17, 2011, the inspectors presented the inspection results to Mr. B. Boles, and other members of the licensee staff. The licensee acknowledged the issues presented. | |||
The inspectors confirmed that none of the potential report input discussed was considered proprietary. | |||
===Exit Meeting Summary=== | ===Exit Meeting Summary=== | ||
ATTACHMENT: | |||
ATTACHMENT: | |||
=SUPPLEMENTAL INFORMATION= | =SUPPLEMENTAL INFORMATION= | ||
==KEY POINTS OF CONTACT== | |||
: [[contact::B. Allen]], Site Vice President | : [[contact::B. Allen]], Site Vice President | ||
Licensee | Licensee | ||
: [[contact::P. Boissoneault; Manager]], Chemistry | : [[contact::P. Boissoneault; Manager]], Chemistry | ||
: [[contact::B. Boles]], Director, Site Operations | : [[contact::B. Boles]], Director, Site Operations | ||
: [[contact::K. Byrd]], Director, Site Performance Improvement | : [[contact::K. Byrd]], Director, Site Performance Improvement | ||
: [[contact::J. Cuff]], Manager, Site Maintenance (Acting) | : [[contact::J. Cuff]], Manager, Site Maintenance (Acting) | ||
: [[contact::J. Dominy]], Director, Site Maintenance | : [[contact::J. Dominy]], Director, Site Maintenance | ||
: [[contact::G. Hayes]], Supervisor, Reactor Engineering | : [[contact::G. Hayes]], Supervisor, Reactor Engineering | ||
: [[contact::J. Hook]], Manager, Design Engineering | : [[contact::J. Hook]], Manager, Design Engineering | ||
: [[contact::V. Kaminskas]], Director, Site Engineering | : [[contact::V. Kaminskas]], Director, Site Engineering | ||
: [[contact::G. Kendrick]], Manager, Site Outage Management | : [[contact::G. Kendrick]], Manager, Site Outage Management | ||
: [[contact::P. McCloskey]], Manager, Site Regulatory Compliance | : [[contact::P. McCloskey]], Manager, Site Regulatory Compliance | ||
: [[contact::D. Noble]], Manager, Radiation Protection | : [[contact::D. Noble]], Manager, Radiation Protection | ||
: [[contact::M. Parker]], Manager, Site Protection | : [[contact::M. Parker]], Manager, Site Protection | ||
: [[contact::R. Patrick]], Manager, Site Work Management | : [[contact::R. Patrick]], Manager, Site Work Management | ||
: [[contact::A. Percival]], Sr. Chemistry Technologist (Liquid Radwaste and Effluent Analysis) | : [[contact::A. Percival]], Sr. Chemistry Technologist (Liquid Radwaste and Effluent Analysis) | ||
: [[contact::S. Plymale]], Manager, Site Operations | : [[contact::S. Plymale]], Manager, Site Operations | ||
: [[contact::J. Sturdavant]], Regulatory Compliance | : [[contact::J. Sturdavant]], Regulatory Compliance | ||
: [[contact::T. Summers]], Manager, Plant Engineering | : [[contact::T. Summers]], Manager, Plant Engineering | ||
: [[contact::J. Vetter]], Manager, Emergency Response | : [[contact::J. Vetter]], Manager, Emergency Response | ||
: [[contact::A. Wise]], Manager, Technical Services | : [[contact::A. Wise]], Manager, Technical Services | ||
: [[contact::D. Kimble]], Senior Resident Inspector | : [[contact::D. Kimble]], Senior Resident Inspector | ||
Nuclear Regulatory Commission | Nuclear Regulatory Commission | ||
==LIST OF ITEMS== | |||
===OPENED, CLOSED AND DISCUSSED=== | |||
None. | |||
LIST OF | |||
===Opened=== | |||
None. | |||
===Closed=== | |||
==LIST OF DOCUMENTS REVIEWED== | |||
}} | }} | ||
Latest revision as of 07:05, 13 January 2025
| ML111091027 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 04/19/2011 |
| From: | Jamnes Cameron NRC/RGN-III/DRP/B6 |
| To: | Allen B FirstEnergy Nuclear Operating Co |
| References | |
| IR-11-008 | |
| Download: ML111091027 (24) | |
Text
April 19, 2011
SUBJECT:
DAVIS-BESSE NUCLEAR POWER STATION - NRC PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION 05000346/2011008
Dear Mr. Allen:
On March 17, 2011, the U.S. Nuclear Regulatory Commission (NRC) completed a Problem Identification and Resolution (PI&R) team inspection at your Davis-Besse Nuclear Power Station. The enclosed report documents the inspection findings, which were discussed on March 17, 2011, with Mr. Brian Boles and other members of your staff.
This inspection was an examination of activities conducted under your license as they relate to the identification and resolution of problems, and compliance with the Commissions rules and regulations and the conditions of your operating license. Within these areas, the inspection involved examination of selected procedures and representative records, observations of activities, and interviews with personnel.
The inspection team concluded that on the basis of the sample selected for review, in general, problems were properly identified, evaluated, and corrected. The team noted that the station staff reviewed operating experience for applicability to station activities. Audits and self-assessments were performed at an appropriate level to identify most deficiencies. Based on the independent assessment of safety culture results, interviews conducted during the inspection, and review of the employee concerns program, freedom to raise nuclear safety concerns was demonstrated.
Based on the results of this inspection, no findings were identified. In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records System (PARS)
component of NRC's document system (ADAMS). ADAMS is accessible from the NRC website at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,
/RA/
Jamnes L. Cameron, Chief Branch 6 Division of Reactor Projects
Docket No. 50-346 License No. NPF-3
Enclosure:
Inspection Report 05000346/2011008 w/Attachment: Supplemental Information
REGION III==
Docket No:
50-346 License No:
NPF-3 Report No:
05000346/2011008 Licensee:
FirstEnergy Nuclear Operating Company (FENOC)
Facility:
Davis-Besse Nuclear Power Station Location:
Oak Harbor, OH Dates:
February 14, 2011, through March 17, 2011 Inspectors:
A. Garmoe, Project Engineer, Team Lead
J. Rutkowski, Senior Resident Inspector,
Davis-Besse, Team Lead
J. Bozga, Reactor Inspector, Mechanical
C. Brown, Reactor Inspector, Electrical
A. Wilson, Resident Inspector
Approved by:
Jamnes L. Cameron, Chief Branch 6 Division of Reactor Projects
Enclosure
SUMMARY OF FINDINGS
IR 05000346/2011008; 02/14/2011 - 03/17/2011; Davis-Besse Nuclear Power Station; Routine
Biennial Problem Identification and Resolution (PI&R) Inspection This inspection was performed by three NRC regional inspectors, one Davis-Besse Nuclear Power Station senior resident inspector, and the Davis-Besse Nuclear Power Station resident inspector. No findings or violations of NRC requirements were identified during this inspection.
The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 4, dated December 2006.
On the basis of the sample selected for review, the team concluded that implementation of the corrective action program (CAP) at Davis-Besse Nuclear Power Station was generally effective.
The licensee had a low threshold for identifying problems and entering them in the CAP. Items entered into the CAP were screened and prioritized in a timely manner using established criteria; were properly evaluated commensurate with their safety significance; and corrective actions were generally implemented in a timely manner, commensurate with the safety significance. The team noted that the licensee reviewed operating experience for applicability to station activities. Audits and self-assessments were determined to be performed at an appropriate level to identify most deficiencies. On the basis of interviews conducted during the inspection, workers at the site expressed freedom to enter safety concerns into the CAP.
Problem Identification and Resolution A.
No findings were identified.
NRC-Identified
and Self-Revealed Findings B.
No violations of significance were identified.
Licensee-Identified Violations
REPORT DETAILS
OTHER ACTIVITIES
4OA2 Problem Identification and Resolution
The activities documented in Sections
.1 through.4 constituted one biennial sample of
problem identification and resolution as defined in Inspection Procedure 71152.
(71152B)
.1 a.
Assessment of the Corrective Action Program Effectiveness The inspectors reviewed the licensees Corrective Action (CA) program implementing procedures and attended CA program meetings to assess the implementation of the CA program by site personnel.
Inspection Scope The inspectors reviewed risk and safety significant issues in the licensees CA program since the last NRC Problem Identification and Resolution (PI&R) inspection in April 2009. The selection of issues ensured an adequate review of issues across NRC cornerstones. The inspectors used issues identified through NRC generic communications, department self assessment, licensee audits, operating experience reports, and NRC documented findings as sources to select issues. Additionally, the inspectors reviewed Condition Reports (CRs) generated as a result of facility personnels performance in daily plant activities. In addition, the inspectors reviewed CRs and a selection of completed investigations from the licensees various investigation methods, which included root cause, full apparent cause, limited apparent cause, and common cause investigations.
The inspectors selected the control rod drive system to review in detail. The inspectors review was to determine whether the licensee staff were properly monitoring and evaluating the performance of these systems through effective implementation of station monitoring programs. A 5 year review on the control rod drive system was undertaken to assess the licensees efforts in monitoring for system degradation due to aging aspects. The inspectors also performed partial system walkdowns of the auxiliary feedwater system and decay heat system. A review of the use of the station maintenance rule program to help identify equipment issues was also conducted.
During the reviews, the inspectors determined whether the licensee staffs actions were in compliance with the facilitys corrective action program and 10 CFR Part 50, Appendix B requirements. Specifically, the inspectors determined whether licensee personnel were identifying plant issues at the proper threshold, entering the plant issues into the stations CA program in a timely manner, and assigning the appropriate prioritization for resolution of the issues. The inspectors also determined whether the licensee staff assigned the appropriate investigation method to ensure the proper determination of root, apparent, and contributing causes. The inspectors also evaluated the timeliness and effectiveness of corrective actions for selected issue reports, completed investigations, and NRC findings, including non-cited violations.
b.
- (1) Assessment Based on the information reviewed, including initiation rates of CRs and interviews, the inspectors concluded that the threshold for initiating condition reports was appropriate.
In addition, the inspectors noted that the licensee trends equipment and human performance on a regular basis.
Effectiveness of Problem Identification The inspectors identified one example of a weakness with regard to entering conditions into the corrective action program at a low threshold. The licensee initiated CR 11-89925 after I&C technicians inadvertently tripped the radwaste ventilation system while performing a surveillance to calibrate radwaste area exhaust process radiation monitor RE5405A. The licensee has been changing out radiation monitors from analog to digital, thus two active procedures were in place to perform the calibration. Prior to calibrating radiation monitor RE5405A, a digital radiation monitor, the technicians were incorrectly provided with the procedure used for calibrating an analog radiation monitor.
The analog procedure performs steps in a slightly different order than the digital procedure, which caused the radwaste ventilation system to trip offline. One of the technicians involved had caught the mistake of being given the wrong procedure on several previous occasions, but did not catch the error in this instance. This event could have been prevented had a condition report been written for the previous instances of being given the wrong procedure.
Observations
No findings were identified.
Findings
- (2) The inspectors reviewed the classification of CRs for resolution and determined that, in general, CRs were assigned appropriate prioritization and evaluation levels and evaluations in apparent cause and root cause reports that were reviewed were adequate.
Effectiveness of Prioritization and Evaluation of Issues
The inspectors reviewed CR 10-75350, Turbine Building HELB Concerns in CCW Pump Room. The inspectors noted that the immediate operability determination was based on engineering judgment that was not numerically or analytically based. Upon further discussion with the Engineering Department, the operability determination was updated to include numerically and analytically based information. The inspectors concluded that the Shift Manager accepted engineering judgment as a basis for operability and did not sufficiently challenge the information provided by Engineering to ensure an adequate basis for operability was provided.
Observations The inspectors also reviewed CR 10-87473, Pipe Stress Calculations for Temporary Shielding. Pipe stress analysis and pipe support calculations were verified to be in conformance with design and licensing basis requirements for decay heat piping systems. However, the inspectors did identify three design control violations of minor significance involving the placement of lead shielding on piping systems. The minor violations were entered into the CA program as CR 11-90280, CR 11-90326, and CR 11-90347.
No findings were identified.
Findings
- (3) In general, the inspectors noted that the corrective actions addressed the cause of the identified problem, and appeared to have been effective in the majority of samples reviewed. The inspectors noted that at least in one department there were some inconsistencies in closing out corrective actions and that those closeouts were not in accordance with station expectations.
Effectiveness of Corrective Actions The inspectors identified several examples where licensee personnel appeared to demonstrate a lack of rigor in complying with stated requirements of the CA program.
Observations Procedure NOP-LP-2001, Corrective Action Program, Section 4.17, states that all approved CAs shall be tracked in the condition report database from initiation until implementation. Additionally, a licensee-generated memorandum sent to Davis-Besse managers on March 10, 2010, re-iterated that CAs identifying that something will be done should not be closed until the action is done. The inspectors reviewed CR 09-55141, Chemistry Plant Status Control Standing Order Noncompliance, and observed that CA #9 was closed on August 26, 2009, with work order system notifications to track remaining open items. Two of the notifications (600566034 and 600566035) were still open as of February 17, 2011. Licensee personnel stated that the CAs were completed but the notifications had not been updated in a timely manner. Additionally, it was identified that CAs #5 and #9 had not been accomplished as written, even though the CAs were closed in the CA program electronic database. As a result of the inspectors observations, the licensee initiated CR 11-89901 and CR 11-89748.
The inspectors reviewed CR 09-67079, Weaknesses in the Boron-10 Correction Factor Program, which was written in response to licensee identified ineffective and incomplete CA from CR 06-06669, Boron 10 Isotopic Composition Not Accounted for in BWST, BAATS, CFTS. Corrective action #3 of CR 09-67079 called for a full review of all Chemistry full and limited apparent causes, dating to 2006, to ensure that all CAs generated as a result of those evaluations were tracked to completion. The results of that review were documented in CR 10-72273, Incomplete Documentation of Corrective Actions, which included several examples of documentation issues or closure issues.
The inspectors noted that the review did not identify that CA #9 from CR 09-55141 had remaining open items.
It was also determined that CA #4 of CR 09-67079 was closed on April 27, 2010, to an action plan that listed actions to be tracked using work order notifications 600612198, 600612199, and 600612200. The action plan stated that the due date for completion of the actions was November 1, 2010. As of February 16, 2011, those notifications were still open even though the licensee stated that the actions had been completed. The licensee documented this issue in CR 11-89741.
The inspectors reviewed CR 10-73290, Unattended Vehicle in the 75 Foot Exclusion Zone near the Dry Fuel Storage Pad, which was written on March 12, 2010, to document a finding issued by the NRC. All CAs and the limited apparent cause analysis were documented as completed as of April 9, 2010. The CR was scheduled to be reviewed by the Corrective Action Review Board (CARB) on November 1, 2010.
However, the sponsoring manager withdrew the document until there was a revised analysis of condition applicability to similar circumstances. As of February 15, 2011, the CR had not been reviewed by the CARB, which is inconsistent with the CARB review time frame requirements of NOP-LP-2001, Corrective Action Program. The licensee initiated CR 11-89733 to document this issue.
The inspectors reviewed CR 09-63254, Finding MS-C-09-08-22: Ineffective Corrective Action Implementation for HSM. The CR discussed a CA from a full apparent cause evaluation (ACE) that had not been effectively implemented. The licensee performed a limited ACE to determine why the CA from the full ACE had not been effectively implemented. The limited ACE identified the cause as a failure to fully follow the CR process; however the inspectors identified that no CA was assigned to address the cause. The inspectors noted that the underlying technical issue, combustible materials within 75 feet of the horizontal storage modules (dry cask spent fuel storage), is an issue that the licensee has not been able to effectively correct for several years. Dating back to 2006, the licensee received two non-cited violations from the NRC and performed numerous apparent cause evaluations. The inspectors view the lack of a CA to address the most recent identified cause, particularly when considered as part of a long-standing issue, as a weakness in the ability to promptly take effective corrective actions.
No findings were identified.
Findings
.2 a.
Assessment of the Use of Operating Experience The inspectors reviewed the licensees implementation of the facilitys Operating Experience (OE) program. Specifically, the inspectors reviewed implementing operating experience program procedures, completed evaluations of OE issues and events, monthly assessments of the OE composite performance indicators, and attended CA program meetings to observe the use of OE information. The inspectors review was to determine whether the licensee was effectively integrating OE experience into the performance of daily activities, whether evaluations of issues were proper and conducted by qualified personnel, whether the licensees program was sufficient to prevent future occurrences of previous industry events, and whether the licensee effectively used the information in developing departmental assessments and facility audits. The inspectors also assessed whether corrective actions, as a result of OE experience, were identified and effectively and timely implemented.
Inspection Scope b.
The inspectors determined that the overall performance of the operating experience program was adequate.
Assessment
The inspectors reviewed the licensees dispositioning of Information Notice (IN) 2008-02, Findings Identified During Component Design Basis Inspections (CDBI), which communicated issues identified during recent CDBI inspections. The inspectors noted that the licensees review of IN 2008-02 was closed to existing procedures and practices, such as the OE Program, Latent Issues Review Process, and the Engineering Design Process. There was very little, if any, applicability review performed by the licensee.
Observations
No findings were identified.
Findings
.3 a.
Assessment of Self-Assessments and Audits The inspectors assessed the licensee staffs ability to identify and enter issues into the CA program, prioritize and evaluate issues, and implement effective CAs, through efforts from departmental assessments and audits.
Inspection Scope b.
The inspectors concluded that self-assessments and audits were typically accurate, thorough, and effective at identifying most issues and enhancement opportunities at an appropriate threshold level. However, the inspectors noted at least one assessment that did not identify issues subsequently identified by the NRC. The inspectors concluded that these audits and self-assessments were completed by personnel knowledgeable in the subject area. In many cases, these self-assessments and audits had identified issues that were not previously recognized by the station.
Assessment Observations The inspectors reviewed licensee self-assessment SN-SA-255, Pre-NRC IP 95001 Inspection Assessment (Davis-Besse EP), for adequacy. The self-assessment was prepared in August 2010, prior to the NRC 95001 supplemental inspection that was conducted in September 2010. The supplemental inspection was conducted in response to a finding of low to moderate (White) safety significance identified in 2009 for the failure to recognize an event in the electrical switchyard that met the emergency action level conditions for declaring an Alert. Self-assessment SN-SA-255 states that the assessment verified that actions taken have been largely effective in correcting the root and contributing causes of the failure to classify. However, the NRC 95001 inspection revealed weaknesses with the adequacy of the licensees extent of cause evaluation and concerns about whether the corrective actions would prevent recurrence.
Site Self Assessments The NRC kept the White finding open until the corrective actions and extent of cause evaluation were expanded. A follow-up NRC 95001 inspection reviewed the updated information and closed the White finding in December 2010. Based on the NRCs concerns during the initial 95001 inspection, the inspectors questioned the adequacy of self-assessment SN-SA-255. The inspectors identified weaknesses in the corrective actions and extent of cause reviews performed by the self-assessment. The licensee initiated CR 11-90395 in response to the inspectors observations.
The inspectors also reviewed self-assessment IP-SA-11-113, Integrated Performance Assessment and Trending for Operations, Second 6 months of 2010. The inspectors identified that the self-assessment failed to identify a trend that was identified by NRC inspectors during the fourth quarter of 2010. Specifically, the NRC integrated fourth quarter Inspection Report 05000356/2010005 identified an adverse trend related to the licensees management of Technical Specifications and Limiting Conditions for Operations, with several examples identified during the third and fourth quarters of 2010.
The inspectors noted a weakness in that self-assessments, including IP-SA-11-113, review NRC inspection reports for findings and violations, but do not review the semi-annual trend review section of the report. A review of the semi-annual trend section could have led the self-assessment to document a potential adverse trend in Operations that was relevant to the second half of 2010.
Self Assessment SN-SA-10-352, Work Order Package Completeness and Associated Impact on the Maintenance Shops, was also reviewed by the inspectors. The licensee conducted this assessment to review why 64 work orders had been placed in Additional Planning status between July 26 and October 4, 2010.
The assessment conclusion did not identify any negative trends attributable to a particular department or process but included the statement, Work Planning needs to continue to strive for increased quality in the work orders. Procedure NOBP-LP-2001, FENOC Self-Assessment/Benchmarking, states that assessment results should be grouped as strengths, recommendations, and deficiencies. Deficiencies and recommendations are required by procedure to have corrective action or notification assignments. The statement referenced was not listed as a deficiency or recommendation and, therefore, had no associated corrective action or notification action that could communicate the insight to plant staff. Discussion with licensee personnel revealed that the need to strive for increased Work Order quality was being reinforced by a corrective action from the Root Cause Evaluation in CR 10-86565, which is not related to SN-SA-10-352. While the concern over work order quality in assessment SN-SA-10-352 was being addressed by a separate unrelated action, the inspectors concluded that, absent the unrelated Root Cause Evaluation, this meaningful observation would have likely not been communicated to plant staff. Such communication could have been accomplished through an assigned corrective action or notification from the self-assessment.
The inspectors reviewed assessments and audits conducted by Fleet Oversight, including the quarterly assessment report from the fourth quarter of 2010. Ratings of the performance of station organizations are assigned by Fleet Oversight in accordance with procedure NOBP-LP-2023, Nuclear Operating Business Practice, Performance Assessment. That procedure specifies four levels of effectiveness using a color scheme of green, white, yellow, and red. In the fourth quarter of 2010, all departments Fleet Oversight Assessments were rated as effective (White), with steady, improved, or improving trends. The inspectors noted several departments were rated as effective for all quarters in 2010.
This included the Chemistry department which, in the fourth quarter of 2010, was rated as marginally effective (Yellow) in a separate assessment, MS-C-10-08-02, a multi-site audit of chemistry and environmental areas. That audit identified recurring significant issues in the laboratory quality control program, failure to satisfy Technical Specification requirements for changes to the Offsite Dose Control Manual, and issues related to chemistry sampling and analysis. The inspectors, while not having a general concern with the overall effectiveness of the assessment and audit program, did question the rating of effective for all station departments.
The inspectors also reviewed Fleet Oversight quarterly assessments for the Site Protection department for the fourth quarter 2009 and all four quarters of 2010, based on review of Condition Report 10-70483, Site Protection Rated Marginally Effective for Fourth Quarter 2009. The assessments show the Site Protection department transitioning from marginally effective (Yellow) to effective (White). The inspectors review of the assessments identified that, when taken as stand-alone documents, it was difficult to verify the conclusions that were reached. The main reason for this appears to be that the assessments focus on different items each quarter, thereby making it more difficult to trend performance. The inspectors did, ultimately, determine that the assessment conclusions were appropriate using information from other performance reports in addition to information included in the quarterly assessments.
The inspectors noted that the licensee-provided listing of assessments did not indicate any assessment of the licensees overall assessment program. The inspectors were advised that such an assessment was scheduled for the second quarter of 2011.
No findings were identified.
Findings
.4 a.
Assessment of Safety Conscious Work Environment The inspectors assessed the licensees safety-conscious work environment (SCWE)through the reviews of the facilitys employee concerns program (ECP) implementing procedures, discussions with the ECP coordinator, interviews with personnel from various departments, and reviews of issue reports. The inspectors also reviewed the results from a 2010 Safety Culture Survey.
Inspection Scope The inspectors interviewed approximately 30 individuals from various departments to assess their willingness to raise nuclear safety issues. The individuals were selected to provide a distribution across the various departments at the site and included long-term contractors. The sample was of individuals predominantly at first-line supervision and below first-line supervision. In addition to assessing individuals willingness to raise nuclear safety issues, the interviews also addressed changes in the CA program and plant environment over the past 2 years. Other items discussed included:
- knowledge and understanding of the CA program;
- effectiveness and efficiency of the CA program;
- willingness to use the CA program;
- managements support of the CA program;
- feedback on issues raised; and
- ease of input to the CA database system.
b.
Interviews indicated that the licensee has an environment where people are free to raise issues without fear of retaliation. Documents provided to the inspectors regarding the 2010 safety culture assessment stated that Davis-Besse Nuclear Power Station maintained a healthy safety culture. Based on a review of the survey data, the inspectors concluded that the data supported that conclusion.
Assessment All interviewees indicated that station personnel would raise safety issues and were comfortable doing so. All individuals knew that, in addition to the CA program, they could raise issues to their management, the ECP, or the NRC. None of the individuals interviewed indicated they had been retaliated against for raising issues nor were they aware of anyone who had been retaliated against. Several interviewees indicated that they believe writing a condition report will result in more work for them and others indicated that condition reports can be perceived negatively by individuals involved in the documented activity. However, all individuals indicated that they would nevertheless raise safety issues through condition reports.
No findings were identified.
Findings 4OA6
.1 Management Meetings
On March 17, 2011, the inspectors presented the inspection results to Mr. B. Boles, and other members of the licensee staff. The licensee acknowledged the issues presented.
The inspectors confirmed that none of the potential report input discussed was considered proprietary.
Exit Meeting Summary
ATTACHMENT:
SUPPLEMENTAL INFORMATION
KEY POINTS OF CONTACT
- B. Allen, Site Vice President
Licensee
- P. Boissoneault; Manager, Chemistry
- B. Boles, Director, Site Operations
- K. Byrd, Director, Site Performance Improvement
- J. Cuff, Manager, Site Maintenance (Acting)
- J. Dominy, Director, Site Maintenance
- G. Hayes, Supervisor, Reactor Engineering
- J. Hook, Manager, Design Engineering
- V. Kaminskas, Director, Site Engineering
- G. Kendrick, Manager, Site Outage Management
- P. McCloskey, Manager, Site Regulatory Compliance
- D. Noble, Manager, Radiation Protection
- M. Parker, Manager, Site Protection
- R. Patrick, Manager, Site Work Management
- A. Percival, Sr. Chemistry Technologist (Liquid Radwaste and Effluent Analysis)
- S. Plymale, Manager, Site Operations
- J. Sturdavant, Regulatory Compliance
- T. Summers, Manager, Plant Engineering
- J. Vetter, Manager, Emergency Response
- A. Wise, Manager, Technical Services
- D. Kimble, Senior Resident Inspector
Nuclear Regulatory Commission
LIST OF ITEMS
OPENED, CLOSED AND DISCUSSED
None.
Opened
None.