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| issue date = 04/30/2014
| issue date = 04/30/2014
| title = IR 05000250-14-002, 05000251-14-002; on 01/01/2014 - 3/31/2014; Turkey Point Nuclear Plant, Units 3 & 4; Problem Identification and Resolution
| title = IR 05000250-14-002, 05000251-14-002; on 01/01/2014 - 3/31/2014; Turkey Point Nuclear Plant, Units 3 & 4; Problem Identification and Resolution
| author name = Croteau R P
| author name = Croteau R
| author affiliation = NRC/RGN-II/DRP
| author affiliation = NRC/RGN-II/DRP
| addressee name = Nazar M
| addressee name = Nazar M
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=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II 245 PEACHTREE CENTER AVENUE NE, SUITE 1200 ATLANTA, GEORGIA 30303-1257 April 30, 2014 EA-14-058
{{#Wiki_filter:April 30, 2014


Mr. Mano Nazar Executive Vice President
==SUBJECT:==
 
TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000250/2014002, 05000251/2014002 AND EXERCISE OF ENFORCEMENT DISCRETION
Nuclear and Chief Nuclear Officer Florida Power and Light Company P.O. Box 14000 Juno Beach, FL 33408-0420
 
SUBJECT: TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000250/2014002, 05000251/2014002 AND EXERCISE OF ENFORCEMENT DISCRETION


==Dear Mr. Nazar:==
==Dear Mr. Nazar:==
On March 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Turkey Point Nuclear Generating Station Units 3 and 4. On April 10, 2014, the NRC inspectors discussed the results of the inspection with Mr. Kiley and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.
On March 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Turkey Point Nuclear Generating Station Units 3 and 4. On April 10, 2014, the NRC inspectors discussed the results of the inspection with Mr. Kiley and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.


NRC inspectors documented two findings of very low safety significance (Green) in this report. The findings involved violations of NRC requirem ents. The NRC is treating these violations as non-cited (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.
NRC inspectors documented two findings of very low safety significance (Green) in this report.
 
In addition, the NRC is exercising enforcement discr etion for two violations of very low safety significance that were not the result of performance deficiencies. Contrary to Technical Specification (TS) 3.7.3, "Intake Cooling Water System," Unit 3 operated in Mode 1 with the 3B intake cooling water pump inoperable for longer than the TS allowed outage time due to a loose fuse holder. Contrary to TS 3.7.2, "Component Cooling Water System," Unit 3 operated in Mode 1 with the 3A component cooling water pump inoperable for longer than the TS allowed outage time due to leakage from the pump casing vent.


Although violations of the TS occurred, the violations were not attributable to equipment failures that were avoidable by reasonable licensee quality assurance measures or management controls. Therefore, the TS 3.7.3 and 3.7.2 violations were not associated with licensee performance deficiencies. The NRC concluded that the violations were of very low safety significance. Based on these facts, I have been authorized, after consultation with the Director, Office of Enforcement, and the Regional Administrator, to exercise enforcement discretion in accordance with Section 2.2.4.d of the Enforcement Policy and refrain from issuing enforcement for the violations. These violations will not be considered in the assessment process or the NRC's Action Matrix. If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at Turkey Point Nuclear Generating Station Units 3 and 4.
The findings involved violations of NRC requirements. The NRC is treating these violations as non-cited (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.


If you disagree with a cross-cutting aspect assignment or the finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II; and the NRC resident inspector at the Turkey Point Nuclear Generating Station Units  
In addition, the NRC is exercising enforcement discretion for two violations of very low safety significance that were not the result of performance deficiencies. Contrary to Technical Specification (TS) 3.7.3, Intake Cooling Water System, Unit 3 operated in Mode 1 with the 3B intake cooling water pump inoperable for longer than the TS allowed outage time due to a loose fuse holder. Contrary to TS 3.7.2, Component Cooling Water System, Unit 3 operated in Mode 1 with the 3A component cooling water pump inoperable for longer than the TS allowed outage time due to leakage from the pump casing vent. Although violations of the TS occurred, the violations were not attributable to equipment failures that were avoidable by reasonable licensee quality assurance measures or management controls. Therefore, the TS 3.7.3 and 3.7.2 violations were not associated with licensee performance deficiencies. The NRC concluded that the violations were of very low safety significance. Based on these facts, I have been authorized, after consultation with the Director, Office of Enforcement, and the Regional Administrator, to exercise enforcement discretion in accordance with Section 2.2.4.d of the Enforcement Policy and refrain from issuing enforcement for the violations. These violations will not be considered in the assessment process or the NRCs Action Matrix. If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at Turkey Point Nuclear Generating Station Units 3 and 4.


3 and 4.
If you disagree with a cross-cutting aspect assignment or the finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II; and the NRC resident inspector at the Turkey Point Nuclear Generating Station Units 3 and 4.


Additionally, as we informed you in the most recent NRC integrated inspection report, cross-cutting aspects identified in the last six months of 2013 using the previous terminology were being converted in accordance with the cross-reference in Inspection Manual Chapter 0310.
Additionally, as we informed you in the most recent NRC integrated inspection report, cross-cutting aspects identified in the last six months of 2013 using the previous terminology were being converted in accordance with the cross-reference in Inspection Manual Chapter 0310.


Section 4OA5 of the enclosed report documents the conversion of these cross-cutting aspects which will be evaluated for cross-cutting themes and potential substantive cross-cutting issues in accordance with IMC 0305 starting with the 2014 mid-cycle assessment review. If you disagree with the cross cutting aspect assigned, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II; and the NRC Resident Inspector at the Turkey Point Nuclear  
Section 4OA5 of the enclosed report documents the conversion of these cross-cutting aspects which will be evaluated for cross-cutting themes and potential substantive cross-cutting issues in accordance with IMC 0305 starting with the 2014 mid-cycle assessment review. If you disagree with the cross cutting aspect assigned, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II; and the NRC Resident Inspector at the Turkey Point Nuclear Generating Station.


Generating Station.
In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding, of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRCs Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
 
In accordance with Title 10 of the Code of Federal Regulations 2.390, "Public Inspections, Exemptions, Requests for Withholding," of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Managem ent System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).


Sincerely,
Sincerely,
/William Jones RA for/  
/William Jones RA for/  


Richard P. Croteau, Director Division of Reactor Projects  
Richard P. Croteau, Director  
 
Division of Reactor Projects  


Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41  
Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41  


Enclosure: Inspection Report 05000250/2014002, 05000251/2014002, w/Attachment: Supplemental Information cc Distribution via ListServ If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at Turkey Point Nuclear Generating Station Units 3 and 4.
===Enclosure:===
Inspection Report 05000250/2014002, 05000251/2014002,  


If you disagree with a cross-cutting aspect assignment or the finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II; and the NRC resident inspector at the Turkey Point Nuclear Generating Station Units
w/Attachment: Supplemental Information


3 and 4.
REGION II==
Docket Nos:


Additionally, as we informed you in the most recent NRC integrated inspection report, cross-cutting aspects identified in the last six months of 2013 using the previous terminology were being converted in accordance with the cross-reference in Inspection Manual Chapter 0310.
50-250, 50-251
 
License Nos:
DPR-31, DPR-41


Section 4OA5 of the enclosed report documents the conversion of these cross-cutting aspects which will be evaluated for cross-cutting themes and potential substantive cross-cutting issues in accordance with IMC 0305 starting with the 2014 mid-cycle assessment review. If you disagree with the cross cutting aspect assigned, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II; and the NRC Resident Inspector at the Turkey Point Nuclear
Report Nos:


Generating Station.
05000250/2014002, 05000251/2014002


In accordance with Title 10 of the Code of Federal Regulations 2.390, "Public Inspections, Exemptions, Requests for Withholding," of the NRC's "Rules of Practice," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Managem ent System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Licensee:  


Sincerely,
Florida Power & Light Company (FP&L)
/William Jones RA for/


Richard P. Croteau, Director Division of Reactor Projects
Facility:


Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41 Enclosure: Inspection Report 05000250/2014002, 05000251/2014002 w/Attachment: Supplemental Information
Turkey Point Nuclear Generating Station, Units 3 & 4


cc Distribution via ListServ PUBLICLY AVAILABLE NON-PUBLICLY AVAILABLE SENSITIVE NON-SENSITIVE ADAMS: Yes ACCESSION NUMBER:_________________________ SUNSI REVIEW COMPLETE FORM 665 ATTACHED OFFICE RII:DRP RII:DRP RII:DRS RII:DRS RII:DRS RII:DRS RII:DRP SIGNATURE Via email Via email Via email Via email Via email Via email SRS5 NAME THoeg MEndress RCarrion MSpeck SSanchez CFontana SSandal DATE 04/25/2014 04/24/2014 04/23/2014 04/23/2014 04/23/2014 04/23/2014 04/24/2014 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO OFFICE RII:ORA RII:DRP RII:DRP SIGNATURE Via email DWR1 WBJ' /RA/ for NAME CEvans DRich RCroteau DATE 04/24/2014 04/29/2014 04/30/2014 5/ /2014 5/ /2014 5/ /2014 5/ /2014 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO Letter to Mano Nazar from Richard Croteau dated April 30, 2014.
Location:  


SUBJECT: TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000250/2014002, 05000251/2014002 AND EXERCISE OF ENFORCEMENT DISCRETION
9760 S. W. 344th Street Homestead, FL 33035


DISTRIBUTION
Dates:  
: C. Evans, RII L. Douglas, RII OE Mail RIDSNRRDIRS


PUBLIC RidsNrrPMTurkeyPoint Resource
January 1 to March 31, 2014


Enclosure U.S. NUCLEAR REGULATORY COMMISSION
Inspectors:


==REGION II==
T. Hoeg, Senior Resident Inspector


Docket Nos: 50-250, 50-251
M. Endress, Resident Inspector


License Nos: DPR-31, DPR-41
M. Speck, Senior Emergency Preparedness Inspector (1EP2-5, 4OA1)


Report Nos: 05000250/2014002, 05000251/2014002
S. Sanchez, Senior Emergency Preparedness Inspector (1EP2-5, 4OA1)


Licensee: Florida Power & Light Company (FP&L)  
C. Fontana, Emergency Preparedness Inspector (1EP2-5, 4OA1)  


Facility: Turkey Point Nuclear Generating Station, Units 3 & 4
R. Carrion, Senior Reactor Inspector (4OA5)


Location: 9760 S. W. 344th Street Homestead, FL 33035 Dates: January 1 to March 31, 2014
Approved by:
Daniel W. Rich, Chief


Inspectors: T. Hoeg, Senior Resident Inspector M. Endress, Resident Inspector M. Speck, Senior Emergency Preparedness Inspector (1EP2-5, 4OA1)
Reactor Projects Branch 3
S. Sanchez, Senior Emergency Preparedness Inspector (1EP2-5, 4OA1)
C. Fontana, Emergency Preparedness Inspector (1EP2-5, 4OA1)
R. Carrion, Senior Reactor Inspector (4OA5)


Approved by: Daniel W. Rich, Chief Reactor Projects Branch 3 Division of Reactor Projects  
Division of Reactor Projects  


Enclosure  
Enclosure  


=SUMMARY OF FINDINGS=
=SUMMARY OF FINDINGS=
IR 05000250/2014002, 05000251/2014002; 01/01/2014 - 3/31/2014; Turkey Point Nuclear Plant, Units 3 & 4; Problem Identification and Resolution.
IR 05000250/2014002, 05000251/2014002; 01/01/2014 - 3/31/2014; Turkey Point Nuclear  


The report covered a three-month period of inspection by the resident inspectors and region-based specialist inspectors. Two Green non-cited violations were identified. The significance of inspection findings are indicated by their color (i.e., Green, White, Yellow, or Red) and determined using Inspection Manual Chapter (IMC) 0609, "Significance Determination Process," (SDP) dated June 2, 2011. The cross-cutting aspects were determined using IMC 0310,  
Plant, Units 3 & 4; Problem Identification and Resolution.
"Components Within the Cross-Cutting Areas," dated December 19, 2013. All violations of NRC requirements were dispositioned in accordance with the NRC's Enforcement Policy dated July 9, 2013. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "R eactor Oversight Process," Revision 5.
 
The report covered a three-month period of inspection by the resident inspectors and region-based specialist inspectors. Two Green non-cited violations were identified. The significance of inspection findings are indicated by their color (i.e., Green, White, Yellow, or Red) and determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process, (SDP) dated June 2, 2011. The cross-cutting aspects were determined using IMC 0310,
Components Within the Cross-Cutting Areas, dated December 19, 2013. All violations of NRC requirements were dispositioned in accordance with the NRCs Enforcement Policy dated July 9, 2013. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision  


===NRC-Identified and Self-Revealing Findings===
===NRC-Identified and Self-Revealing Findings===
===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
* Green: A self-revealing non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, was identified when the licensee failed to implement corrective actions that addressed the low stress high cycle fatigue of component cooling water (CCW) relief valve (RV) 4-747B piping caused by flow induced vibration. As a result, CCW system flow induced vibration resulted in weld cracks and system pressure boundary leakage in January 2014. This issue was placed in the licensee's corrective action program (CAP) as action request (AR) 1931761. Corrective actions included performing a root cause evaluation, implementing special instructions to minimize the time that split header operation is performed, and developing a plan to replace the existing relief valve with an orifice or alternate relief valve.
* Green: A self-revealing non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI,
Corrective Action, was identified when the licensee failed to implement corrective actions that addressed the low stress high cycle fatigue of component cooling water (CCW) relief valve (RV) 4-747B piping caused by flow induced vibration. As a result, CCW system flow induced vibration resulted in weld cracks and system pressure boundary leakage in January 2014. This issue was placed in the licensees corrective action program (CAP) as action request (AR) 1931761. Corrective actions included performing a root cause evaluation, implementing special instructions to minimize the time that split header operation is performed, and developing a plan to replace the existing relief valve with an orifice or alternate relief valve.


The performance deficiency was more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to implement adequate corrective actions to address CCW system flow induced vibration resulted in weld cracks and CCW system pressure boundary leakage in January 2014. The finding was screened using Exhibit 1, Mitigating Systems Screening Questions, found in Inspection Manual Chapter 0609, Significance Determination Process, Appendix A, Significance Determination Process (SDP) for Findings At-Power (June 19, 2012). The inspectors determined the finding was of very low safety significance (Green) because the finding did not affect design or qualification, did not represent a loss of system function, and did not represent an actual loss of function of a TS train of equipment. The finding was associated with a cross-cutting aspect in the evaluation component of the problem identification and resolution area because the licensee did not thoroughly evaluate issues and corrective actions from previous weld failures on CCW system RV-4-747B piping caused by flow induced vibration (P.2). (Section 4OA2.2)
The performance deficiency was more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to implement adequate corrective actions to address CCW system flow induced vibration resulted in weld cracks and CCW system pressure boundary leakage in January 2014. The finding was screened using Exhibit 1, Mitigating Systems Screening Questions, found in Inspection Manual Chapter 0609, Significance Determination Process, Appendix A,
* Green: A self-revealing non-cited violation (NCV) of TS Section 3.3.2, "Engineered Safety Features Actuation Instrumentation," (ESF) was identified when the licensee failed to perform the channel calibration of Unit 3 ESF steam pressure protection channel III within the required 18-month frequency which resulted in operation with steam generator pressure transmitter PT-3-495 inoperable for approximately 10 months. This issue was placed in the licensee's CAP as AR 1938191. Corrective actions included replacing PT-3-495, performing an extent of condition on all other work orders completed during the extended power uprate (EPU) outage to ensure TS compliance, and revising the surveillance tracking program procedure to require verification that the required surveillance testing is completed prior to crediting non-dedicated work orders.
Significance Determination Process (SDP) for Findings At-Power (June 19, 2012). The inspectors determined the finding was of very low safety significance (Green) because the finding did not affect design or qualification, did not represent a loss of system function, and did not represent an actual loss of function of a TS train of equipment. The finding was associated with a cross-cutting aspect in the evaluation component of the problem identification and resolution area because the licensee did not thoroughly evaluate issues and corrective actions from previous weld failures on CCW system RV-4-747B piping caused by flow induced vibration (P.2). (Section 4OA2.2)
* Green: A self-revealing non-cited violation (NCV) of TS Section 3.3.2, Engineered Safety Features Actuation Instrumentation, (ESF) was identified when the licensee failed to perform the channel calibration of Unit 3 ESF steam pressure protection channel III within the required 18-month frequency which resulted in operation with steam generator pressure transmitter PT-3-495 inoperable for approximately 10 months. This issue was placed in the licensees CAP as AR 1938191. Corrective actions included replacing PT-3-495, performing an extent of condition on all other work orders completed during the extended power uprate (EPU) outage to ensure TS compliance, and revising the surveillance tracking program procedure to require verification that the required surveillance testing is completed prior to crediting non-dedicated work orders.


The performance deficiency was more than minor because it was associated with the human performance attribute of the mitigating systems cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to perform the channel calibration surveillance test procedure for transmitter PT-3-495 within the 18-month required frequency resulted in 10 months of channel inoperability. The finding was screened using Exhibit 1, Mitigating Systems Screening Questions, found in Inspection Manual Chapter 0609, Significance Determination Process, Appendix A, Significance Determination Process for Findings At-Power (June 19, 2012). The inspectors determined the finding was of very low safety significance (Green) because the finding did not affect design or qualification, did not represent a loss of system function, and did not represent an actual loss of function of a technical specification train of equipment. The finding was associated with a cross-cutting aspect in the work management component of the human performance area because the licensee failed to implement their process for planning, controlling, and executing required surveillance tests (H.5). (Section 4OA2.3)
The performance deficiency was more than minor because it was associated with the human performance attribute of the mitigating systems cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to perform the channel calibration surveillance test procedure for transmitter PT-3-495 within the 18-month required frequency resulted in 10 months of channel inoperability. The finding was screened using Exhibit 1, Mitigating Systems Screening Questions, found in Inspection Manual Chapter 0609, Significance Determination Process, Appendix A, Significance Determination Process for Findings At-Power (June 19, 2012). The inspectors determined the finding was of very low safety significance (Green) because the finding did not affect design or qualification, did not represent a loss of system function, and did not represent an actual loss of function of a technical specification train of equipment. The finding was associated with a cross-cutting aspect in the work management component of the human performance area because the licensee failed to implement their process for planning, controlling, and executing required surveillance tests (H.5). (Section 4OA2.3)  
 
===
 
Licensee Identified Violations===


===Licensee Identified Violations===
None
None


Line 135: Line 131:


===Summary of Plant Status===
===Summary of Plant Status===
Unit 3 began this inspection period at 100 percent of rated thermal power (RTP) where it remained until March 17 when it was shut down for a planned refueling outage that continued through the end of this inspection period.
Unit 3 began this inspection period at 100 percent of rated thermal power (RTP) where it remained until March 17 when it was shut down for a planned refueling outage that continued through the end of this inspection period.


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==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity (R)  
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity (R)  
{{a|1R04}}


{{a|1R04}}
==1R04 Equipment Alignment
==1R04 Equipment Alignment==


==
===.1 Partial Equipment Walk Downs (Quarterly)===
===.1 Partial Equipment Walk Downs (Quarterly)===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted three partial alignment verifications of the safety-related systems listed below. These inspections included reviews using plant lineup procedures, operating procedures, and piping and instrumentation drawings, which were compared with observed equipment configurations to verify that the critical portions of the systems were correctly aligned to support operability. The inspectors also verified that the licensee had identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers by entering them into the CAP. Documents reviewed are listed in the Attachment.
The inspectors conducted three partial alignment verifications of the safety-related systems listed below. These inspections included reviews using plant lineup procedures, operating procedures, and piping and instrumentation drawings, which were compared with observed equipment configurations to verify that the critical portions of the systems were correctly aligned to support operability. The inspectors also verified that the licensee had identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers by entering them into the CAP. Documents reviewed are listed in the Attachment.
Line 158: Line 153:


===.2 Equipment Alignment (Semi-annual)===
===.2 Equipment Alignment (Semi-annual)===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted a detailed review of the alignment and material condition of the A standby feed water system train to verify its capability to meet its design basis function while the B standby feed water system was OOS for troubleshooting and repair.
The inspectors conducted a detailed review of the alignment and material condition of the A standby feed water system train to verify its capability to meet its design basis function while the B standby feed water system was OOS for troubleshooting and repair.


The inspectors utilized licensee procedure 0-OSP-074.3, "Standby Steam Generator Feedwater Pumps Availability" and Drawings 5610-M-3074, "Feedwater System," Sheets 1 and 2, to verify the system alignment was correct. During the walkdown, the inspectors verified, as appropriate, that: 1) valves were correctly positioned and did not exhibit leakage that would impact their function, 2) electrical power was available as required, 3) major portions of the system and components were correctly labeled, cooled, and ventilated, 4) hangers and supports were correctly installed and functional, 5) essential support systems were operational, 6) ancillary equipment or debris did not interfere with system performance, 7) tagging clearances were appropriate, and 8)valves were locked as required by the licensee's locked valve program. Other items reviewed included the operator workaround list, the temporary modification list, system health reports, system description, and open maintenance work orders. In addition, the inspectors reviewed the licensee's CAP to ensure that the licensee was identifying and resolving associated equipment problems.
The inspectors utilized licensee procedure 0-OSP-074.3, Standby Steam Generator Feedwater Pumps Availability and Drawings 5610-M-3074, Feedwater System, Sheets 1 and 2, to verify the system alignment was correct. During the walkdown, the inspectors verified, as appropriate, that: 1) valves were correctly positioned and did not exhibit leakage that would impact their function, 2) electrical power was available as required, 3) major portions of the system and components were correctly labeled, cooled, and ventilated, 4) hangers and supports were correctly installed and functional, 5) essential support systems were operational, 6) ancillary equipment or debris did not interfere with system performance, 7) tagging clearances were appropriate, and 8)valves were locked as required by the licensees locked valve program. Other items reviewed included the operator workaround list, the temporary modification list, system health reports, system description, and open maintenance work orders. In addition, the inspectors reviewed the licensees CAP to ensure that the licensee was identifying and resolving associated equipment problems.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
{{a|1R05}}
 
==1R05 Fire Protection==
==1R05 Fire Protection


==
===.1 Fire Area Walk downs===
===.1 Fire Area Walk downs===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors toured the following five plant areas to evaluate conditions related to control of transient combustibles, ignition sources, material condition, and operational status of fire protection systems including fire barriers used to prevent fire damage and propagation. The inspectors reviewed these activities using provisions in the licensee's procedure 0-ADM-016, "Fire Protection Plan" and 10 CFR Part 50, Appendix R. The licensee's fire impairment lists were routinely reviewed. In addition, the inspectors reviewed the condition report database to verify that fire protection problems were being identified and appropriately resolved. The inspectors accompanied fire watch roving personnel on a tour of fire protection impairments and risk significant fire areas to assure monitoring of area status and to verify proper identification and handling of transient combustibles. The following areas were inspected:
The inspectors toured the following five plant areas to evaluate conditions related to control of transient combustibles, ignition sources, material condition, and operational status of fire protection systems including fire barriers used to prevent fire damage and propagation. The inspectors reviewed these activities using provisions in the licensees procedure 0-ADM-016, Fire Protection Plan and 10 CFR Part 50, Appendix R. The licensees fire impairment lists were routinely reviewed. In addition, the inspectors reviewed the condition report database to verify that fire protection problems were being identified and appropriately resolved. The inspectors accompanied fire watch roving personnel on a tour of fire protection impairments and risk significant fire areas to assure monitoring of area status and to verify proper identification and handling of transient combustibles. The following areas were inspected:
* DC Equipment Room 4B Fire Zone 101
* DC Equipment Room 4B Fire Zone 101
* DC Equipment Room 3A Fire Zone 104
* DC Equipment Room 3A Fire Zone 104
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====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R07}}
{{a|1R07}}
 
==1R07 Heat Sink Performance==
==1R07 Heat Sink Performance


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors selected the 3A component cooling water heat exchanger to verify the licensee was performing periodic cleaning and inspections to ensure its tubes remained clear and unobstructed. The inspectors observed portions of the heat exchanger cleaning and inspection performed by the licensee under WO 40295368. The inspectors verified the cleaning and inspection was performed and properly documented in accordance with completed maintenance procedure 0-PMM-030.01, "Component Cooling Water Heat Exchanger Cleaning and Inspection.The inspectors also reviewed completed licensee procedure 3-OSP-019.4, "Component Cooling Water Heat Exchanger Performance Monitoring" to ensure the heat exchanger was restored, leak tested, and returned to service with no deficiencies.
==
The inspectors selected the 3A component cooling water heat exchanger to verify the licensee was performing periodic cleaning and inspections to ensure its tubes remained clear and unobstructed. The inspectors observed portions of the heat exchanger cleaning and inspection performed by the licensee under WO 40295368. The inspectors verified the cleaning and inspection was performed and properly documented in accordance with completed maintenance procedure 0-PMM-030.01, Component Cooling Water Heat Exchanger Cleaning and Inspection. The inspectors also reviewed completed licensee procedure 3-OSP-019.4, Component Cooling Water Heat Exchanger Performance Monitoring to ensure the heat exchanger was restored, leak tested, and returned to service with no deficiencies.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R11}}
{{a|1R11}}
 
==1R11 Licensed Operator Requalification Program==
==1R11 Licensed Operator Requalification Program  


Resident Inspector Quarterly Review
Resident Inspector Quarterly Review


==
===.1 Simulator Observations===
===.1 Simulator Observations===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors performed the following two inspection samples of simulator observations and assessed licensed operator performance while training. These observations included procedural use and adherence, response to alarms, communications, command and control, and coordination and control of the reactor plant operations.
The inspectors performed the following two inspection samples of simulator observations and assessed licensed operator performance while training. These observations included procedural use and adherence, response to alarms, communications, command and control, and coordination and control of the reactor plant operations.


On February 6, 2014, the inspectors assessed licensed operator performance in the plant-specific simulator during an emergency preparedness drill scenario. The training scenario was started with the unit at 100 percent power and steady state conditions. Event simulations consisted of damage to an irradiated fuel assembly in the spent fuel pit, a large break loss of coolant accident (LOCA), and anticipated transient without scram (ATWS). Operators responded to the simulation using off-normal procedures 3-ONOP-067, Radioactive Effluent Release, and 3-ONOP-041.4, Excessive Reactor Coolant System Activity. Emergency procedures used by the crew to safely mitigate the events included 3-EOP-E-0, Reactor Trip and 3-EOP-FR-S-1, Response to Nuclear Power Generation ATWS. The inspectors specifically checked that the simulated emergency classifications of Alert and General Emergency were done in accordance with licensee procedure, 0-EPIP-20101, Duties of the Emergency Coordinator.
On February 6, 2014, the inspectors assessed licensed operator performance in the plant-specific simulator during an emergency preparedness drill scenario. The training scenario was started with the unit at 100 percent power and steady state conditions.
 
Event simulations consisted of damage to an irradiated fuel assembly in the spent fuel pit, a large break loss of coolant accident (LOCA), and anticipated transient without scram (ATWS). Operators responded to the simulation using off-normal procedures 3-ONOP-067, Radioactive Effluent Release, and 3-ONOP-041.4, Excessive Reactor Coolant System Activity. Emergency procedures used by the crew to safely mitigate the events included 3-EOP-E-0, Reactor Trip and 3-EOP-FR-S-1, Response to Nuclear Power Generation ATWS. The inspectors specifically checked that the simulated emergency classifications of Alert and General Emergency were done in accordance with licensee procedure, 0-EPIP-20101, Duties of the Emergency Coordinator.


On March 12, 2014, the inspectors observed and assessed operator training associated with an upcoming refueling outage on Unit 3 scheduled for March 17, 2014. The licensed operators participated in "just in time training" for collapsing a pressurizer bubble and transition to solid pressure control in accordance with procedure 3-NOP-041.02, Pressurizer Operation.
On March 12, 2014, the inspectors observed and assessed operator training associated with an upcoming refueling outage on Unit 3 scheduled for March 17, 2014. The licensed operators participated in just in time training for collapsing a pressurizer bubble and transition to solid pressure control in accordance with procedure 3-NOP-041.02, Pressurizer Operation.


During these simulator observations, the simulator board configurations were compared with actual plant control board configurations concerning recent power up rate modifications. The inspectors specifically evaluated the following attributes related to operating crew performance and the licensee evaluation:
During these simulator observations, the simulator board configurations were compared with actual plant control board configurations concerning recent power up rate modifications. The inspectors specifically evaluated the following attributes related to operating crew performance and the licensee evaluation:
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* Oversight and direction provided by shift supervisor, including ability to identify and implement appropriate TS actions and emergency plan classification and notification
* Oversight and direction provided by shift supervisor, including ability to identify and implement appropriate TS actions and emergency plan classification and notification
* Crew overall performance and interactions
* Crew overall performance and interactions
* Evaluator's control of the scenario and post scenario evaluation of crew performance
* Evaluators control of the scenario and post scenario evaluation of crew performance


====b. Findings====
====b. Findings====
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===.2 Control Room Observations===
===.2 Control Room Observations===
====a. Inspection Scope====
The inspectors performed the following focused control room observations and assessed licensed operator performance in the control room. These observations included daily routine surveillance testing, response to alarms, communications, shift turnovers, and coordination of plant activities. These observations were conducted to verify operator compliance with station operating guidelines, such as use of procedures, control and manipulation of components, and communications. On March 5, 2014, the inspectors did a focused observation on Unit 4 consisting of a reactor coolant system primary water dilution per 0-OP-046, Enclosure 6, Chemical Volume Control System Boron Concentration Control. Specifically, the inspectors observed the reactor operators performing the pre-job brief per 0-ADM-200, Attachment 7, Planned Reactivity Manipulations for Maintaining Steady State Plant Conditions and verified the operators complied with the applicable procedure during the evolution.


====a. Inspection Scope====
The inspectors focused on the following conduct of operations attributes as  
The inspectors performed the following focused control room observations and assessed licensed operator performance in the control room. These observations included daily routine surveillance testing, response to alarms, communications, shift turnovers, and coordination of plant activities. These observations were conducted to verify operator compliance with station operating guidelines, such as use of procedures, control and manipulation of components, and communications. On March 5, 2014, the inspectors did a focused observation on Unit 4 consisting of a reactor coolant system primary water dilution per 0-OP-046, Enclosure 6, "Chemical Volume Control System Boron Concentration Control."  Specifically, the inspectors observed the reactor operators performing the pre-job brief per 0-ADM-200, Attachment 7, "Planned Reactivity Manipulations for Maintaining Steady State Plant Conditions" and verified the operators complied with the applicable procedure during the evolution.


The inspectors focused on the following conduct of operations attributes as  appropriate:
appropriate:
* Operator compliance and use of procedures
* Operator compliance and use of procedures
* Control board manipulations
* Control board manipulations
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====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R12}}
{{a|1R12}}
 
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed known equipment problems associated with the 4C component cooling water pump and the R-4-11 containment radiation monitor affecting the maintenance rule program and equipment performance history trends associated with the equipment. The inspectors reviewed the licensee's activities to meet the requirements of 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, and licensee procedure NAP-415, "Maintenance Rule Program Administration.The inspectors focused on maintenance rule scoping, characterization of maintenance problems and failed components, risk significance, determination of a(1) or a(2) performance criteria classification, corrective actions, and the appropriateness of established performance goals and monitoring criteria. The inspectors also interviewed responsible engineers and observed or reviewed corrective maintenance activities. The inspectors verified that equipment problems were being identified and appropriately entered into the licensee's CAP. The inspectors used the licensee maintenance rule data base, system health reports, maintenance rule unavailability status reports, and the CAP as sources of information on tracking and resolution of issues.
==
The inspectors reviewed known equipment problems associated with the 4C component cooling water pump and the R-4-11 containment radiation monitor affecting the maintenance rule program and equipment performance history trends associated with the equipment. The inspectors reviewed the licensees activities to meet the requirements of 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, and licensee procedure NAP-415, Maintenance Rule Program Administration. The inspectors focused on maintenance rule scoping, characterization of maintenance problems and failed components, risk significance, determination of a(1) or a(2) performance criteria classification, corrective actions, and the appropriateness of established performance goals and monitoring criteria. The inspectors also interviewed responsible engineers and observed or reviewed corrective maintenance activities. The inspectors verified that equipment problems were being identified and appropriately entered into the licensees CAP. The inspectors used the licensee maintenance rule data base, system health reports, maintenance rule unavailability status reports, and the CAP as sources of information on tracking and resolution of issues.
* 4C Component Cooling Water Pump Unavailability, AR 01942801
* 4C Component Cooling Water Pump Unavailability, AR 01942801
* R-4-11 Containment Radiation Monitor Unavailability, AR 01946565
* R-4-11 Containment Radiation Monitor Unavailability, AR 01946565


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R13}}
{{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors completed in-office reviews and control room inspections of the licensee's risk assessment of four emergent or planned maintenance activities. The inspectors verified the licensee's risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and procedures 0-ADM-068, "Work Week Management;" WM-AA-1000, "Work Ac tivity Risk Management;" and O-ADM-225, "On Line Risk Assessment and Management.The inspectors also reviewed the effectiveness of the licensee's contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee assessment of aggregate risk using procedure OP-AA-104-1007, "Online Aggregate Risk.The inspectors discussed the on-line risk monitor (OLRM) results with the control room operators and verified all applicable out of service equipment was included in the OLRM calculation. The inspectors evaluated the following four risk assessments during the inspection period:
==
The inspectors completed in-office reviews and control room inspections of the licensees risk assessment of four emergent or planned maintenance activities. The inspectors verified the licensees risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and procedures 0-ADM-068, Work Week Management; WM-AA-1000, Work Activity Risk Management; and O-ADM-225, On Line Risk Assessment and Management. The inspectors also reviewed the effectiveness of the licensees contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee assessment of aggregate risk using procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors discussed the on-line risk monitor (OLRM) results with the control room operators and verified all applicable out of service equipment was included in the OLRM calculation. The inspectors evaluated the following four risk assessments during the inspection period:
* 3B Intake Cooling Water (ICW) pump, 4A High Head Safety Injection (HHSI) pump, and Auxiliary Feed Water (AFW) Train 2 OOS
* 3B Intake Cooling Water (ICW) pump, 4A High Head Safety Injection (HHSI) pump, and Auxiliary Feed Water (AFW) Train 2 OOS
* 3A Component Cooling Water (CCW) Heat Exchanger, 3B CCW Pump, and 3C Coolant Charging Pump OOS
* 3A Component Cooling Water (CCW) Heat Exchanger, 3B CCW Pump, and 3C Coolant Charging Pump OOS
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====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R15}}
{{a|1R15}}
 
==1R15 Operability Determinations and Functionality Assessments==
==1R15 Operability Determinations and Functionality Assessments


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the technical adequacy of licensee evaluations to ensure that TS operability was properly justified and t he subject component or system remained available such that no unrecognized increase in risk occurred for the five operability evaluations described in the ARs listed below. The inspectors reviewed applicable sections of the UFSAR to determine if the system or component remained available to perform its intended function. In addition, when applicable, the inspectors reviewed compensatory measures implemented to verify that the affected equipment remained capable of performing its design function. The inspectors also reviewed a sampling of condition reports to verify that the licensee was routinely identifying and correcting any deficiencies associated with operability evaluations.
==
The inspectors evaluated the technical adequacy of licensee evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred for the five operability evaluations described in the ARs listed below. The inspectors reviewed applicable sections of the UFSAR to determine if the system or component remained available to perform its intended function. In addition, when applicable, the inspectors reviewed compensatory measures implemented to verify that the affected equipment remained capable of performing its design function. The inspectors also reviewed a sampling of condition reports to verify that the licensee was routinely identifying and correcting any deficiencies associated with operability evaluations.
* AR 1931750, Missed Technical Specification Surveillances
* AR 1931750, Missed Technical Specification Surveillances
* AR 1931761, Unit 4 CCW Piping Failure
* AR 1931761, Unit 4 CCW Piping Failure
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====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R18}}
{{a|1R18}}
 
==1R18 Plant Modifications==
==1R18 Plant Modifications  


Temporary Plant Modifications
Temporary Plant Modifications


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed a temporary plant modification technical evaluation for leaving a robot in the containment building 14 foot elevation while at full power. The robot became stuck when one of its tracks became dislodged from its wheels while being used in an attempt to identify secondary plant leakage inside the containment bio-wall. The inspectors reviewed the 10 CFR 50.59 screening and technical evaluation to verify that the modification had not affected system operability or availability. The inspectors reviewed associated plant drawings and UFSAR documents impacted by this modification and discussed the changes with licensee personnel to verify that the installation was consistent with the modification documents. The inspectors reviewed photographs of the robot location to determine if conditions resulted in any potential unsafe conditions not described in the engineering change documentation. Additionally, the inspectors verified that problems associated with modifications were being identified  
==
 
The inspectors reviewed a temporary plant modification technical evaluation for leaving a robot in the containment building 14 foot elevation while at full power. The robot became stuck when one of its tracks became dislodged from its wheels while being used in an attempt to identify secondary plant leakage inside the containment bio-wall. The inspectors reviewed the 10 CFR 50.59 screening and technical evaluation to verify that the modification had not affected system operability or availability. The inspectors reviewed associated plant drawings and UFSAR documents impacted by this modification and discussed the changes with licensee personnel to verify that the installation was consistent with the modification documents. The inspectors reviewed photographs of the robot location to determine if conditions resulted in any potential unsafe conditions not described in the engineering change documentation. Additionally, the inspectors verified that problems associated with modifications were being identified and entered into the CAP.
and entered into the CAP.
* EC 281021, Irretrievable Robot in U4 Containment
* EC 281021, Irretrievable Robot in U4 Containment


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R19}}
{{a|1R19}}
 
==1R19 Post Maintenance Testing==
==1R19 Post Maintenance Testing


====a. Inspection Scope====
====a. Inspection Scope====
For the five post maintenance tests and associated work orders (WO) listed below, the inspectors reviewed the test procedures and either witnessed the testing or reviewed test records to determine whether the scope of testing adequately verified that the work performed was correctly completed and demonstrated that the affected equipment was operable. The inspectors verified that the requirements in licensee procedure 0-ADM-737, "Post Maintenance Testing," were incorporated into the test requirements. The inspectors reviewed the following WOs consisting of three inspection samples:
==
For the five post maintenance tests and associated work orders (WO) listed below, the inspectors reviewed the test procedures and either witnessed the testing or reviewed test records to determine whether the scope of testing adequately verified that the work performed was correctly completed and demonstrated that the affected equipment was operable. The inspectors verified that the requirements in licensee procedure 0-ADM-737, Post Maintenance Testing, were incorporated into the test requirements. The inspectors reviewed the following WOs consisting of three inspection samples:
* WO 40166635, 3A EDG on line maintenance
* WO 40166635, 3A EDG on line maintenance
* WO 40288777, Unit 4 RV-4-747B pipe repair
* WO 40288777, Unit 4 RV-4-747B pipe repair
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====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R20}}
{{a|1R20}}
 
==1R20 Refueling and Other Outage Activities==
==1R20 Refueling and Other Outage Activities  


Unit 3 Refueling Outage PT3-27
Unit 3 Refueling Outage PT3-27


====a. Inspection Scope====
====a. Inspection Scope====
Outage Planning, Control and Risk Assessment During daily outage planning activities by the licensee, the inspectors reviewed the risk reduction methodology employed by the licensee during various refueling outage (RFO)
==
PT3-27 meetings including outage control center (OCC) morning meetings, operations daily team meetings, and schedule performance update meetings. The inspectors examined the licensee implementation of shutdown safety assessments during PT3-27 in accordance with administrative procedure ADM-51, "Outage Risk Assessment and Control," to verify if a defense in depth concept was in place to ensure safe operations and avoid unnecessary risk. In addition, the inspectors regularly monitored outage planning and control activities in the OCC, and interviewed responsible OCC management personnel during the outage to ensure system, structure, and component configurations, and work scope were consistent with TS requirements, site procedures, and outage risk controls.
Outage Planning, Control and Risk Assessment  
 
During daily outage planning activities by the licensee, the inspectors reviewed the risk reduction methodology employed by the licensee during various refueling outage (RFO)
PT3-27 meetings including outage control center (OCC) morning meetings, operations daily team meetings, and schedule performance update meetings. The inspectors examined the licensee implementation of shutdown safety assessments during PT3-27 in accordance with administrative procedure ADM-51, Outage Risk Assessment and Control, to verify if a defense in depth concept was in place to ensure safe operations and avoid unnecessary risk. In addition, the inspectors regularly monitored outage planning and control activities in the OCC, and interviewed responsible OCC management personnel during the outage to ensure system, structure, and component configurations, and work scope were consistent with TS requirements, site procedures, and outage risk controls.


Shutdown, Cooldown, and Transition to Mode 5 Activities
Shutdown, Cooldown, and Transition to Mode 5 Activities  


The inspectors observed selected Unit 3 shutdown, cooldown, and mode transition activities starting on March 17, 2014. The inspectors verified that activities were performed in accordance with the outage plan and associated plant procedures. The inspectors evaluated specific performance attributes including operator performance, communications, and risk management. The inspectors evaluated the following activities:
The inspectors observed selected Unit 3 shutdown, cooldown, and mode transition activities starting on March 17, 2014. The inspectors verified that activities were performed in accordance with the outage plan and associated plant procedures. The inspectors evaluated specific performance attributes including operator performance, communications, and risk management. The inspectors evaluated the following activities:
* Monitored decay heat removal system performance, lineups, and cooldown rates.
* Monitored decay heat removal system performance, lineups, and cooldown rates.
* Verified that the plant cooldown was conducted in accordance with licensee procedure 3-OSP-041.7, Reactor Coolant System Heatup and Cooldown Temperature Verification Monitoring of Shutdown Activities The inspectors performed walkdowns of important systems and components used for decay heat removal from the spent fuel pool during the shutdown period including the intake cooling water system, component cooling water system, and spent fuel pool cooling system.
* Verified that the plant cooldown was conducted in accordance with licensee procedure 3-OSP-041.7, Reactor Coolant System Heatup and Cooldown Temperature Verification  
 
Monitoring of Shutdown Activities  


Outage Activities The inspectors examined outage activities to verify that they were conducted in accordance with TS, licensee procedures, and the licensee's outage risk control plan.
The inspectors performed walkdowns of important systems and components used for decay heat removal from the spent fuel pool during the shutdown period including the intake cooling water system, component cooling water system, and spent fuel pool cooling system.
 
Outage Activities  
 
The inspectors examined outage activities to verify that they were conducted in accordance with TS, licensee procedures, and the licensees outage risk control plan.


Some of the more significant inspection activities accomplished by the inspectors were as follows:
Some of the more significant inspection activities accomplished by the inspectors were as follows:
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* Reviewed control of containment penetrations
* Reviewed control of containment penetrations
* Examined foreign material exclusion (FME) controls put in place inside containment (e.g., around the refueling cavity, near sensitive equipment and RCS breaches) and around the spent fuel pool (SFP)
* Examined foreign material exclusion (FME) controls put in place inside containment (e.g., around the refueling cavity, near sensitive equipment and RCS breaches) and around the spent fuel pool (SFP)
* Verified workers fatigue rule was properly managed Refueling Activities and Containment Closure The inspectors witnessed selected fuel handling operations being performed in accordance with TS and applicable operating procedures from the main control room, refueling cavity inside containment, and the spent fuel pool bridge. The inspectors also examined licensee activities to control and track the position of each fuel assembly. The inspectors evaluated the licensee's ability to close the containment equipment, personnel, and emergency hatches in a timely manner per procedure 2-MMP-68.02, Containment Closure.
* Verified workers fatigue rule was properly managed  


Corrective Action Program The inspectors reviewed ARs generated during PT3-27 to evaluate the licensee's threshold for initiating ARs. The inspectors reviewed CRs to verify priorities, mode holds, and significance levels were assigned as required. Resolution and implementation of corrective actions of several ARs were also reviewed for completeness. The inspectors routinely reviewed the results of quality assurance (QA)daily surveillances of outage activities.
Refueling Activities and Containment Closure
 
The inspectors witnessed selected fuel handling operations being performed in accordance with TS and applicable operating procedures from the main control room, refueling cavity inside containment, and the spent fuel pool bridge. The inspectors also examined licensee activities to control and track the position of each fuel assembly. The inspectors evaluated the licensees ability to close the containment equipment, personnel, and emergency hatches in a timely manner per procedure 2-MMP-68.02, Containment Closure.
 
Corrective Action Program  
 
The inspectors reviewed ARs generated during PT3-27 to evaluate the licensees threshold for initiating ARs. The inspectors reviewed CRs to verify priorities, mode holds, and significance levels were assigned as required. Resolution and implementation of corrective actions of several ARs were also reviewed for completeness. The inspectors routinely reviewed the results of quality assurance (QA)daily surveillances of outage activities.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R22}}
{{a|1R22}}
 
==1R22 Surveillance Testing==
==1R22 Surveillance Testing


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors either reviewed or observed the following five surveillance tests to verify that the tests met the TS requirements, the UFSAR description, the licensee's procedural requirements, and demonstrated the systems were capable of performing their intended safety functions and operational readiness. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the status required for the system to perform its safety function. The inspectors verified that surveillance issues were documented in the licensee's CAP. The inspectors reviewed the following tests:
==
The inspectors either reviewed or observed the following five surveillance tests to verify that the tests met the TS requirements, the UFSAR description, the licensees procedural requirements, and demonstrated the systems were capable of performing their intended safety functions and operational readiness. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the status required for the system to perform its safety function. The inspectors verified that surveillance issues were documented in the licensees CAP. The inspectors reviewed the following tests:  


Surveillance Test
Surveillance Test:
:
* 3-OSP-023.1, 3A EDG monthly test
* 3-OSP-023.1, 3A EDG monthly test
* 4-OSP-059.1, Unit 4 quadrant power tilt ratio (QPTR)
* 4-OSP-059.1, Unit 4 quadrant power tilt ratio (QPTR)
* 4-OSP-023.1, 4B EDG monthly test In-Service Tests
* 4-OSP-023.1, 4B EDG monthly test  
:
 
In-Service Tests:
* 4-OSP-055.1, 4C emergency containment cooler (ECC) quarterly valve in-service test (IST)
* 4-OSP-055.1, 4C emergency containment cooler (ECC) quarterly valve in-service test (IST)
RCS Leak Detection Test
RCS Leak Detection Test:
:
* 3-OSP-041.1, Unit 3 reactor coolant system leak rate calculation
* 3-OSP-041.1, Unit 3 reactor coolant system leak rate calculation


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.  
 
===Cornerstone:  Emergency Preparedness (EP)===


===Cornerstone: Emergency Preparedness (EP)===
1EP2 Alert and Notification System Evaluation
1EP2 Alert and Notification System Evaluation


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the adequacy of the licensee's methods for testing the alert and notification system in accordance with NRC Inspection Procedure 71114, Attachment 02, Alert and Notification System (ANS) Testing. The applicable planning standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50, Appendix E, Section  
The inspectors evaluated the adequacy of the licensees methods for testing the alert and notification system in accordance with NRC Inspection Procedure 71114, 02, Alert and Notification System (ANS) Testing. The applicable planning standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50, Appendix E, Section IV.D requirements were used as reference criteria. The criteria contained in NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, were also used as a reference.


IV.D requirements were used as reference criteria. The criteria contained in NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, were also used as a reference.
The inspectors reviewed various documents which are listed in the Attachment.


The inspectors reviewed various documents which are listed in the Attachment. Inspectors interviewed personnel involved with siren system maintenance and observed annual siren maintenance field activities. This inspection activity satisfied one inspection sample for the alert and notification system on a biennial basis.
Inspectors interviewed personnel involved with siren system maintenance and observed annual siren maintenance field activities. This inspection activity satisfied one inspection sample for the alert and notification system on a biennial basis.


====b. Findings====
====b. Findings====
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the licensee's Emergency Response Organization (ERO)augmentation staffing requirements and process for notifying the ERO to ensure the readiness of key staff for responding to an event and timely facility activation. The qualification records of key position ERO personnel were reviewed to ensure all ERO qualifications were current. A sample of problems identified from augmentation drills or system tests performed since the last inspection was reviewed to assess the effectiveness of corrective actions.
The inspectors reviewed the licensees Emergency Response Organization (ERO)augmentation staffing requirements and process for notifying the ERO to ensure the readiness of key staff for responding to an event and timely facility activation. The qualification records of key position ERO personnel were reviewed to ensure all ERO qualifications were current. A sample of problems identified from augmentation drills or system tests performed since the last inspection was reviewed to assess the effectiveness of corrective actions.


The inspection was conducted in accor dance with NRC Inspection Procedure 71114, Attachment 03, Emergency Preparedness Organization Staffing and Augmentation System. The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR 50, Appendix E requirements were used as reference criteria.
The inspection was conducted in accordance with NRC Inspection Procedure 71114, 03, Emergency Preparedness Organization Staffing and Augmentation System. The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR 50, Appendix E requirements were used as reference criteria.


The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the ERO staffing and augmentation system on a biennial basis.
The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the ERO staffing and augmentation system on a biennial basis.
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====a. Inspection Scope====
====a. Inspection Scope====
Since the last NRC inspection of this pr ogram area, no changes have been made to the Radiological Emergency Plan or Emergency Action Levels. The licensee did make several changes to emergency plan implementing procedures and determined that, in accordance with 10 CFR 50.54(q), the changes made in these revisions resulted in no reduction in the effectiveness of the Plan, and that the Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors conducted a sampling of the implementing procedure changes made between September 1, 2013, and January 15, 2014, to evaluate for potential reductions in the effectiveness of the Plan. However, this review was not documented in a Safety Evaluation Report and does not constitute formal NRC approval of the changes.
Since the last NRC inspection of this program area, no changes have been made to the Radiological Emergency Plan or Emergency Action Levels. The licensee did make several changes to emergency plan implementing procedures and determined that, in accordance with 10 CFR 50.54(q), the changes made in these revisions resulted in no reduction in the effectiveness of the Plan, and that the Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors conducted a sampling of the implementing procedure changes made between September 1, 2013, and January 15, 2014, to evaluate for potential reductions in the effectiveness of the Plan. However, this review was not documented in a Safety Evaluation Report and does not constitute formal NRC approval of the changes.


Therefore, these changes remain subject to future NRC inspection in their entirety.
Therefore, these changes remain subject to future NRC inspection in their entirety.


The inspection was conducted in accor dance with NRC Inspection Procedure 71114, Attachment 04, Emergency Action Level and Emergency Plan Changes. The applicable planning standards of 10 CFR 50.47(b), and its related requirements in 10 CFR 50, Appendix E, were used as reference criteria.
The inspection was conducted in accordance with NRC Inspection Procedure 71114, 04, Emergency Action Level and Emergency Plan Changes. The applicable planning standards of 10 CFR 50.47(b), and its related requirements in 10 CFR 50, Appendix E, were used as reference criteria.


The inspectors reviewed various documents that are listed in the Attachment to this report. This inspection activity satisfied one inspection sample for the emergency action level and emergency plan changes on an annual basis.
The inspectors reviewed various documents that are listed in the Attachment to this report. This inspection activity satisfied one inspection sample for the emergency action level and emergency plan changes on an annual basis.
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====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed the corrective actions identified through the Emergency Preparedness program to determine the significance of the issues, the completeness and effectiveness of corrective actions, and to determine if issues were recurring. The licensee's post-event action reports, self-assessments, and audits were reviewed to assess the licensee's ability to be self-critical, thus avoiding complacency and degradation of their emergency preparedness program. Inspectors reviewed the licensee's 10 CFR 50.54(q) change process, personnel training, and selected screenings and evaluations to assess adequacy. The inspectors toured facilities and reviewed equipment and facility maintenance records to assess licensee's adequacy in maintaining them. The inspectors evaluated the capabilities of selected radiation monitoring instrumentation to adequately support Emergency Action Level (EAL)  
The inspectors reviewed the corrective actions identified through the Emergency Preparedness program to determine the significance of the issues, the completeness and effectiveness of corrective actions, and to determine if issues were recurring. The licensees post-event action reports, self-assessments, and audits were reviewed to assess the licensees ability to be self-critical, thus avoiding complacency and degradation of their emergency preparedness program. Inspectors reviewed the licensees 10 CFR 50.54(q) change process, personnel training, and selected screenings and evaluations to assess adequacy. The inspectors toured facilities and reviewed equipment and facility maintenance records to assess licensees adequacy in maintaining them. The inspectors evaluated the capabilities of selected radiation monitoring instrumentation to adequately support Emergency Action Level (EAL)declarations.
 
declarations.


The inspection was conducted in accordanc e with NRC Inspection Procedure 71114.05, Maintenance of Emergency Preparedness. The applicable planning standards, related 10 CFR 50, Appendix E requirements, and 10 CFR 50.54(q) and
The inspection was conducted in accordance with NRC Inspection Procedure 71114.05, Maintenance of Emergency Preparedness. The applicable planning standards, related 10 CFR 50, Appendix E requirements, and 10 CFR 50.54(q) and
: (t) were used as reference criteria.
: (t) were used as reference criteria.


The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the maintenance of emergency preparedness on a biennial basis.
The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the maintenance of emergency preparedness on a biennial basis.


1EP6 Drill Evaluation Emergency Preparedness Drill
1EP6 Drill Evaluation  
 
Emergency Preparedness Drill


====a. Inspection Scope====
====a. Inspection Scope====
On February 6, 2014, the inspectors observed an emergency preparedness drill and the performance of the licensee's emergency response organization. The drill included a simulated damaged irradiated fuel assembly in the spent fuel pit of Unit 3, a failed steam pressure transmitter resulting in a transient that resulting in a fuel barrier failure. The fuel barrier failure required a site area emergency declaration and notification to state and local county officials, and the NRC per licensee procedure 0-EPIP-20101, Duties of the Emergency Coordinator. The scenario progressed to the loss of the reactor coolant pressure boundary barrier after a large break loss of coolant accident occurred requiring a general emergency declaration and an additional notification. The inspectors observed the crew in the plant simulator including simulated implementation of emergency procedures. The inspectors observed the emergency response organization staff in the technical support center (TSC) and emergency operations facility (EOF) while they implemented the event classifi cation guidelines and emergency response procedures. The inspectors determined that the emergency classification and notifications were made in accordance with the licensee emergency plan implementing procedure 0-EPIP-20101. The inspectors attended the licensee's post drill critique, reviewed the licensee's critique items, and discussed inspector observations with the licensee to verify that drill issues were identified and captured in the licensee's corrective action program.
On February 6, 2014, the inspectors observed an emergency preparedness drill and the performance of the licensees emergency response organization. The drill included a simulated damaged irradiated fuel assembly in the spent fuel pit of Unit 3, a failed steam pressure transmitter resulting in a transient that resulting in a fuel barrier failure. The fuel barrier failure required a site area emergency declaration and notification to state and local county officials, and the NRC per licensee procedure 0-EPIP-20101, Duties of the Emergency Coordinator. The scenario progressed to the loss of the reactor coolant pressure boundary barrier after a large break loss of coolant accident occurred requiring a general emergency declaration and an additional notification. The inspectors observed the crew in the plant simulator including simulated implementation of emergency procedures. The inspectors observed the emergency response organization staff in the technical support center (TSC) and emergency operations facility (EOF) while they implemented the event classification guidelines and emergency response procedures. The inspectors determined that the emergency classification and notifications were made in accordance with the licensee emergency plan implementing procedure 0-EPIP-20101. The inspectors attended the licensees post drill critique, reviewed the licensees critique items, and discussed inspector observations with the licensee to verify that drill issues were identified and captured in the licensees corrective action program.


====b. Findings====
====b. Findings====
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==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification (IP 71151)==
==4OA1 Performance Indicator Verification (IP 71151)==
===.1 Initiating Events Cornerstone===
===.1 Initiating Events Cornerstone===
====a. Inspection Scope====
The inspectors reviewed licensee submittals for the Unit 3 and Unit 4 performance indicators (PI) listed below for the period January 1, 2013, through December 31, 2013, to verify the accuracy of the PI data reported during that period. Performance indicator definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedure 0-ADM-032, NRC Performance Indicators Turkey Point, were used to check the reporting for each data element. The inspectors checked operator logs, plant status reports, condition reports, system health reports, and PI data sheets to verify that the licensee had identified the required data, as applicable.


====a. Inspection Scope====
The inspectors interviewed licensee personnel associated with performance indicator data collection, evaluation, and distribution.
The inspectors reviewed licensee submittals for the Unit 3 and Unit 4 performance indicators (PI) listed below for the period January 1, 2013, through December 31, 2013, to verify the accuracy of the PI data reported during that period. Performance indicator definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," and licensee procedure 0-ADM-032, "NRC Performance Indicators Turkey Point," were used to check the reporting for each data element. The inspectors checked operator logs, plant status reports, condition reports, system health reports, and PI data sheets to verify that the licensee had identified the required data, as applicable. The inspectors interviewed licensee personnel associated with performance indicator data collection, evaluation, and distribution.
* Unit 3 Unplanned Scrams per 7000 Critical Hours
* Unit 3 Unplanned Scrams per 7000 Critical Hours
* Unit 4 Unplanned Scrams per 7000 Critical Hours
* Unit 4 Unplanned Scrams per 7000 Critical Hours
Line 423: Line 439:


===.2 Emergency Preparedness Cornerstone===
===.2 Emergency Preparedness Cornerstone===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors sampled licensee submittals relative to the PIs listed below for the period April 1, 2013, through September 30, 2013. To verify the accuracy of the PI data reported during that period, PI definitions and guidance contained in NEI 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 6, were used to confirm the reporting basis for each data element.
The inspectors sampled licensee submittals relative to the PIs listed below for the period April 1, 2013, through September 30, 2013. To verify the accuracy of the PI data reported during that period, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were used to confirm the reporting basis for each data element.
* Emergency Response Organization (ERO) Drill/Exercise Performance
* Emergency Response Organization (ERO) Drill/Exercise Performance
* ERO Drill Participation
* ERO Drill Participation
* Alert and Notification System Reliability For the specified review period, the inspectors examined data reported to the NRC, procedural guidance for reporting PI information, and records used by the licensee to identify potential PI occurrences. The inspectors verified the accuracy of the PI for ERO drill and exercise performance through review of a sample of drill and event records. The inspectors reviewed selected training records to verify the accuracy of the PI for ERO drill participation for personnel assigned to key positions in the ERO. The inspectors verified the accuracy of the PI for alert and notification system reliability through review of a sample of the licensee's records of periodic system tests. The inspectors also interviewed the licensee personnel who were responsible for collecting and evaluating the PI data. Licensee procedures, records, and other documents reviewed within this inspection area are listed in the Attachment. This inspection satisfied three inspection samples for PI verification on an annual basis.
* Alert and Notification System Reliability  
 
For the specified review period, the inspectors examined data reported to the NRC, procedural guidance for reporting PI information, and records used by the licensee to identify potential PI occurrences. The inspectors verified the accuracy of the PI for ERO drill and exercise performance through review of a sample of drill and event records.
 
The inspectors reviewed selected training records to verify the accuracy of the PI for ERO drill participation for personnel assigned to key positions in the ERO. The inspectors verified the accuracy of the PI for alert and notification system reliability through review of a sample of the licensees records of periodic system tests. The inspectors also interviewed the licensee personnel who were responsible for collecting and evaluating the PI data. Licensee procedures, records, and other documents reviewed within this inspection area are listed in the Attachment. This inspection satisfied three inspection samples for PI verification on an annual basis.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.
{{a|4OA2}}


{{a|4OA2}}
==4OA2 Problem Identification and Resolution (IP 71152)==
==4OA2 Problem Identification and Resolution (IP 71152)==
===.1 Daily Review===
===.1 Daily Review===
====a. Inspection Scope====
====a. Inspection Scope====
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensee's corrective action program. This review was accomplished by reviewing daily printed summaries of ARs and by reviewing the licensee's electronic AR database.
As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensees corrective action program. This review was accomplished by reviewing daily printed summaries of ARs and by reviewing the licensees electronic AR database.


Additionally, RCS unidentified leakage was checked on a daily basis to verify no substantive or unexplained changes. Documents reviewed are listed in the Attachment.
Additionally, RCS unidentified leakage was checked on a daily basis to verify no substantive or unexplained changes. Documents reviewed are listed in the Attachment.
Line 450: Line 467:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors selected the root cause evaluation for AR 01931761, "CCW Pipe Leak Upstream of RV-4-747B, 4B RHR Heat Exchanger Return Relief Valve," for a more in-depth review of the circumstances and the corrective actions that followed. The root cause report was reviewed to ensure that an appropriate evaluation was performed and corrective actions were specified and prioritized in accordance with the licensee's program. Other attributes checked included disposition of operability and resolution of the problem including cause determination and corrective actions. The inspectors evaluated the condition report in accordance with the requirements of the licensee's corrective actions process as specified in licensee's procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action.
The inspectors selected the root cause evaluation for AR 01931761, CCW Pipe Leak Upstream of RV-4-747B, 4B RHR Heat Exchanger Return Relief Valve, for a more in-depth review of the circumstances and the corrective actions that followed. The root cause report was reviewed to ensure that an appropriate evaluation was performed and corrective actions were specified and prioritized in accordance with the licensees program. Other attributes checked included disposition of operability and resolution of the problem including cause determination and corrective actions. The inspectors evaluated the condition report in accordance with the requirements of the licensees corrective actions process as specified in licensees procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action.


====b. Findings and Observations====
====b. Findings and Observations====
=====Introduction:=====
=====Introduction:=====
A Green self-revealing non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, was identified when the licensee failed to implement corrective actions that addressed the low stress high cycle fatigue of component cooling water (CCW) relief valve RV-4-747B piping caused by flow induced vibration. As a result, CCW system flow induced vibration resulted in weld cracks and system pressure boundary leakage in January 2014.
A Green self-revealing non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, was identified when the licensee failed to implement corrective actions that addressed the low stress high cycle fatigue of component cooling water (CCW) relief valve RV-4-747B piping caused by flow induced vibration. As a result, CCW system flow induced vibration resulted in weld cracks and system pressure boundary leakage in January 2014.


=====Description:=====
=====Description:=====
On November 18, 2012, plant personnel identified a weld leak of 5 to 10 drops per minute at the relief valve RV-4-747B piping branch connection on the 16 inch CCW piping. This leak was at the same location where the weld had been previously repaired in November 2011. The licensee entered the leak into the CAP as AR 1824939 and performed an apparent cause evaluation which concluded that there was significant movement of the Unit 4 CCW relief valve RV-4-747B piping while residual heat removal (RHR) was in service. Failure of the weld was due to low stress high cycle fatigue caused by flow induced vibration. In February 2013, the licensee repaired the branch connection weld leak while Unit 4 was in a refueling outage. A corrective action was assigned to engineering to evaluate the need for pipe supports to reduce the effects from the flow induced vibration on the piping. A pipe support was installed in June 2013 at RV-4-747B under engineering change (EC) 278231; however, the analysis used to design the support did not validate the effectiveness of the support to reduce vibration effects to an acceptable level. On January 8, 2014, plant operations identified a 0.0024 gallon per minute leak on the toe of the weld on the half coupling connection between the 1 inch piping upstream of RV-4-747B and 16 inch CCW discharge pipe of the 4B RHR heat exchanger. This leak location was in the same location as the previous leaks identified in 2011 and 2012. The licensee entered the leak into the CAP as AR 1931761 and performed a root cause evaluation which concluded the failure mechanism of the cracked weld was the same as the previous weld failure in 2012 and 2011 which was low stress high cycle fatigue. The cause of the fatigue was determined to be elevated system pressure transients during pump in-service tests combined with potentially degraded relief valve operation which resulted in excessive vibration in the 1 inch relief  
On November 18, 2012, plant personnel identified a weld leak of 5 to 10 drops per minute at the relief valve RV-4-747B piping branch connection on the 16 inch CCW piping. This leak was at the same location where the weld had been previously repaired in November 2011. The licensee entered the leak into the CAP as AR 1824939 and performed an apparent cause evaluation which concluded that there was significant movement of the Unit 4 CCW relief valve RV-4-747B piping while residual heat removal (RHR) was in service. Failure of the weld was due to low stress high cycle fatigue caused by flow induced vibration. In February 2013, the licensee repaired the branch connection weld leak while Unit 4 was in a refueling outage. A corrective action was assigned to engineering to evaluate the need for pipe supports to reduce the effects from the flow induced vibration on the piping. A pipe support was installed in June 2013 at RV-4-747B under engineering change (EC) 278231; however, the analysis used to design the support did not validate the effectiveness of the support to reduce vibration effects to an acceptable level. On January 8, 2014, plant operations identified a 0.0024 gallon per minute leak on the toe of the weld on the half coupling connection between the 1 inch piping upstream of RV-4-747B and 16 inch CCW discharge pipe of the 4B RHR heat exchanger. This leak location was in the same location as the previous leaks identified in 2011 and 2012. The licensee entered the leak into the CAP as AR 1931761 and performed a root cause evaluation which concluded the failure mechanism of the cracked weld was the same as the previous weld failure in 2012 and 2011 which was low stress high cycle fatigue. The cause of the fatigue was determined to be elevated system pressure transients during pump in-service tests combined with potentially degraded relief valve operation which resulted in excessive vibration in the 1 inch relief valve inlet line.
 
valve inlet line.


=====Analysis:=====
=====Analysis:=====
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=====Enforcement:=====
=====Enforcement:=====
10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires in part that measures shall be established to assure conditions adverse to quality are promptly identified and corrected. Contrary to the above, in November 2011 and November 2012, the licensee identified that the 4B CCW relief valve piping to the 4B RHR heat exchanger experienced system pressure boundary leakage due to low stress high cycle fatigue caused by flow induced vibration on the line, but failed to implement corrective actions that addressed the flow induced vibration. The failure to correct the flow induced vibration resulted in a weld failure in the CCW relief valve piping in January 2014. The licensee repaired the weld failures, implemented special instructions to minimize the time that split header operation was performed, and developed a plan to replace the existing relief valve with an orifice or alternate relief valve. This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy, because it was of very low safety significance and was entered in the licensee's corrective action program as AR 1931761 to address recurrence. (NCV 05000251/2014002-01 Failure to Take Adequate Corrective Actions to Correct Flow Induced Vibration Leads to CCW Piping Weld Failure).
10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires in part that measures shall be established to assure conditions adverse to quality are promptly identified and corrected. Contrary to the above, in November 2011 and November 2012, the licensee identified that the 4B CCW relief valve piping to the 4B RHR heat exchanger experienced system pressure boundary leakage due to low stress high cycle fatigue caused by flow induced vibration on the line, but failed to implement corrective actions that addressed the flow induced vibration. The failure to correct the flow induced vibration resulted in a weld failure in the CCW relief valve piping in January 2014. The licensee repaired the weld failures, implemented special instructions to minimize the time that split header operation was performed, and developed a plan to replace the existing relief valve with an orifice or alternate relief valve. This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy, because it was of very low safety significance and was entered in the licensees corrective action program as AR 1931761 to address recurrence. (NCV 05000251/2014002-01 Failure to Take Adequate Corrective Actions to Correct Flow Induced Vibration Leads to CCW Piping Weld Failure).


===.3 Annual Sample:===
===.3 Annual Sample:===
Line 472: Line 486:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors selected root cause evaluation for AR 01930745, "PT-3-495 found out of calibration during 3-SMI-072.02," for a more in-depth review of the circumstances and the corrective actions that followed. The root cause report was reviewed to ensure that an appropriate evaluation was performed and corrective actions were specified and prioritized in accordance with the licensee's program. Other attributes checked included disposition of operability and resolution of the problem including cause determination and corrective actions. The inspectors evaluated the condition report in accordance with the requirements of the licensee's corrective actions process as specified in licensee's procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action.
The inspectors selected root cause evaluation for AR 01930745, PT-3-495 found out of calibration during 3-SMI-072.02, for a more in-depth review of the circumstances and the corrective actions that followed. The root cause report was reviewed to ensure that an appropriate evaluation was performed and corrective actions were specified and prioritized in accordance with the licensees program. Other attributes checked included disposition of operability and resolution of the problem including cause determination and corrective actions. The inspectors evaluated the condition report in accordance with the requirements of the licensees corrective actions process as specified in licensees procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action.


====b. Findings and Observations====
====b. Findings and Observations====
=====Introduction:=====
=====Introduction:=====
A Green self-revealing non-cited violation (NCV) of TS Section 3.3.2, "Engineered Safety Features Actuation Instrumentation," (ESF) was identified when the licensee failed to perform the channel calibration of Unit 3 ESF steam pressure protection channel III within the required 18-month frequency. When the surveillance was performed, the licensee determined that steam generator pressure transmitter PT-3-495 needed to be replaced due to excessive drift. The licensee considered PT-3-495 to have been inoperable for approximately 10 months going back to the original due date of the channel calibration.
A Green self-revealing non-cited violation (NCV) of TS Section 3.3.2, Engineered Safety Features Actuation Instrumentation, (ESF) was identified when the licensee failed to perform the channel calibration of Unit 3 ESF steam pressure protection channel III within the required 18-month frequency. When the surveillance was performed, the licensee determined that steam generator pressure transmitter PT-3-495 needed to be replaced due to excessive drift. The licensee considered PT-3-495 to have been inoperable for approximately 10 months going back to the original due date of the channel calibration.


=====Description:=====
=====Description:=====
On December 13, 2013, during the performance of a functionality review for an unrelated issue, it became readily apparent to the licensee that channel calibration procedure 3-SMI-072.2, "P-3-466, P-3-475, P-3-485, and P-3-495 Steam Pressure Channel Calibration, Protection Channels," had not been performed for approximately 31 months. Technical Specification 3.3.2 and Table 4.3-2 required that a channel calibration be performed on channels with input to ESF every 18 months. On April 15, 2013, during the Unit 3 extended power uprate (EPU) outage, the licensee credited completion of the Unit 3 main steam line pressure transmitter channel calibration for P-3-495 in the surveillance tracking program (STP) in error. The licensee normally tracked completion of TS surveillance requirements by completion of dedicated work orders, but in this case a partial performance of the channel calibration was imbedded in a larger work order. On discovery of the missed channel calibration, the licensee applied the provision of TS 4.0.3 for a missed TS surveillance test of P-3-495. Accordingly, the licensee performed a risk evaluation which determined that completion of the surveillance could be delayed up to the specified 18-month surveillance interval for the test without a significant increase in risk to the plant. In October 2013, the licensee  
On December 13, 2013, during the performance of a functionality review for an unrelated issue, it became readily apparent to the licensee that channel calibration procedure 3-SMI-072.2, P-3-466, P-3-475, P-3-485, and P-3-495 Steam Pressure Channel Calibration, Protection Channels, had not been performed for approximately 31 months. Technical Specification 3.3.2 and Table 4.3-2 required that a channel calibration be performed on channels with input to ESF every 18 months. On April 15, 2013, during the Unit 3 extended power uprate (EPU) outage, the licensee credited completion of the Unit 3 main steam line pressure transmitter channel calibration for P-3-495 in the surveillance tracking program (STP) in error. The licensee normally tracked completion of TS surveillance requirements by completion of dedicated work orders, but in this case a partial performance of the channel calibration was imbedded in a larger work order. On discovery of the missed channel calibration, the licensee applied the provision of TS 4.0.3 for a missed TS surveillance test of P-3-495. Accordingly, the licensee performed a risk evaluation which determined that completion of the surveillance could be delayed up to the specified 18-month surveillance interval for the test without a significant increase in risk to the plant. In October 2013, the licensee performed loss of fill oil preventive maintenance (PM) check 003PM095033, U3 Rosemount Transmitter Surveillance Program, for P-3-495 and identified that the transmitter needed to be calibrated or replaced as soon as possible based on increasing drift. The licensee generated an AR to track replacement of the transmitter, but the AR was canceled and scheduled by maintenance to be replaced the next time the instrument was removed from service. The inspectors observed that the licensees missed surveillance risk evaluation for P-3-495 did not consider the degradation identified during this October PM task. On January 3, 2014, while performing 3-SMI-072.2 for Unit 3 steam break protection channel III, main steam line pressure transmitter PT-3-495 was found outside of the procedural acceptance criteria due to pressure transmitter drift. Transmitter PT-3-495 provides the C steam generator channel III pressure signal used for the ESF steam line isolation signal to mitigate a steam break design basis accident. Transmitter PT-3-495 was replaced, calibrated successfully, and returned to service on January 4, 2014. The licensee determined that the transmitter and associated instrument channel were inoperable from March 9, 2013 (the time of the due date for the missed surveillance), until the date of repair. The licensee concluded that the overall ESF steam pressure protection signal was operable since both redundant steam pressure protection channels II and IV remained available and were demonstrated to be operable by the successful performance of their respective surveillances. During the period of inoperability, the instrument channel associated with PT-3-495, Channel III remained in service and exceeded the allowed outage time of 6 hours to place the channel in the tripped condition and the shutdown actions of TS 3.0.3 were not entered. As a result, the licensee submitted LER 05000250/2014-001-00 in accordance with 10CFR50.73(a)(2)(i)(B) as a condition prohibited by TS. The inspectors determined that the issue was self-revealing because the condition became readily apparent to the licensee during the performance of a functionality review for an unrelated issue. Additionally, the inspectors concluded that the licensee had missed an opportunity to address degradation of the instrument following the completion of the October 2013 PM.


performed 'loss of fill oil' preventive maintenance (PM) check 003PM095033, "U3 Rosemount Transmitter Surveillance Program," for P-3-495 and identified that the transmitter needed to be calibrated or replaced as soon as possible based on increasing drift. The licensee generated an AR to track replacement of the transmitter, but the AR was canceled and scheduled by maintenance to be replaced the next time the instrument was removed from service. The inspectors observed that the licensee's missed surveillance risk evaluation for P-3-495 did not consider the degradation identified during this October PM task. On January 3, 2014, while performing 3-SMI-072.2 for Unit 3 steam break protection channel III, main steam line pressure transmitter PT-3-495 was found outside of the procedural acceptance criteria due to pressure
The licensees root cause evaluation (RCE) determined the cause of this event to be the deviation from the normal process of using a dedicated work order (WO) to satisfy surveillance requirements. This created a situation where there was no second verifier to ensure that surveillance test requirements had been satisfactorily completed. This issue was placed in the licensees CAP as AR 1938191. Corrective actions completed (or planned) included:
 
transmitter drift. Transmitter PT-3-495 provides the 'C' steam generator channel III pressure signal used for the ESF steam line isolation signal to mitigate a steam break design basis accident. Transmitter PT-3-495 was replaced, calibrated successfully, and returned to service on January 4, 2014. The licensee determined that the transmitter and associated instrument channel were inoperable from March 9, 2013 (the time of the due date for the missed surveillance), until the date of repair. The licensee concluded that the overall ESF steam pressure protection signal was operable since both redundant steam pressure protection channels II and IV remained available and were demonstrated to be operable by the successful performance of their respective surveillances. During the period of inoperability, the instrument channel associated with PT-3-495, Channel III remained in service and exceeded the allowed outage time of 6 hours to place the channel in the tripped condition and the shutdown actions of TS 3.0.3
 
were not entered. As a result, the licensee submitted LER 05000250/2014-001-00 in accordance with 10CFR50.73(a)(2)(i)(B) as a condition prohibited by TS. The inspectors determined that the issue was self-revea ling because the condition became readily apparent to the licensee during the performance of a functionality review for an unrelated issue. Additionally, the inspectors concluded that the licensee had missed an opportunity to address degradation of the instrument following the completion of the October 2013 PM.
 
The licensee's root cause evaluation (RCE) determined the cause of this event to be the deviation from the normal process of using a dedicated work order (WO) to satisfy surveillance requirements. This created a situation where there was no second verifier to ensure that surveillance test requirements had been satisfactorily completed. This  
 
issue was placed in the licensee's CAP as AR 1938191. Corrective actions completed (or planned) included:
: (1) replacing PT-3-495,
: (1) replacing PT-3-495,
: (2) performing an extent of condition on all other work orders completed during the extended power uprate (EPU) outage to ensure TS compliance and
: (2) performing an extent of condition on all other work orders completed during the extended power uprate (EPU) outage to ensure TS compliance and
: (3) revising the surveillance tracking program procedure to verify that a surveillance test has been completed when crediting non-dedicated work  
: (3) revising the surveillance tracking program procedure to verify that a surveillance test has been completed when crediting non-dedicated work orders.
 
orders.


=====Analysis:=====
=====Analysis:=====
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=====Enforcement:=====
=====Enforcement:=====
Turkey Point Nuclear Plant Unit 3 TS surveillance requirement 3.3.2, "Engineered Safety Features Actuation Instrumentation," Table 4.3-2 requires in part that instrument operability be demonstrated by successful completion of a channel calibration of the ESF steam line pressure protection channel every 18 months. If the instrument channel is determined to be inoperable, TS 3.3.2 allows continued operation until the next required performance of the analog channel operational test provided that the inoperable channel is placed in trip within six hours. Contrary to the above, from April 25, 2011, to January 3, 2014, Turkey Point failed to perform the required channel calibration of Unit 3 steam line protection channel III, and failed to perform the required actions of TS LCO 3.3.2 when operability was no longer supported on March 9, 2013.
Turkey Point Nuclear Plant Unit 3 TS surveillance requirement 3.3.2, Engineered Safety Features Actuation Instrumentation, Table 4.3-2 requires in part that instrument operability be demonstrated by successful completion of a channel calibration of the ESF steam line pressure protection channel every 18 months. If the instrument channel is determined to be inoperable, TS 3.3.2 allows continued operation until the next required performance of the analog channel operational test provided that the inoperable channel is placed in trip within six hours. Contrary to the above, from April 25, 2011, to January 3, 2014, Turkey Point failed to perform the required channel calibration of Unit 3 steam line protection channel III, and failed to perform the required actions of TS LCO 3.3.2 when operability was no longer supported on March 9, 2013.


This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy. The violation was entered into the licensee's CAP as AR 1938191 (NCV 05000250/2014002-02 TS Channel Calibration of ESF Steam Line Protection Channel III Not Performed).
This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy. The violation was entered into the licensees CAP as AR 1938191 (NCV 05000250/2014002-02 TS Channel Calibration of ESF Steam Line Protection Channel III Not Performed).


{{a|4OA3}}
{{a|4OA3}}
==4OA3 Follow-up of Events and Notice of Enforcement Discretion (IP 71153)==
==4OA3 Follow-up of Events and Notice of Enforcement Discretion (IP 71153)==
 
===.1 (Closed) Licensee Event Report (LER) 05000250/2013-009-00, Loose Breaker Control===
===.1 (Closed) Licensee Event Report (LER) 05000250/2013-009-00, Loose Breaker Control Power Fuse Holder Caused 3B ICW Pump to be Inoperable Longer than Allowed Outage===
Power Fuse Holder Caused 3B ICW Pump to be Inoperable Longer than Allowed Outage Time
 
Time


====a. Inspection Scope====
====a. Inspection Scope====
The LER documented that the 3B Intake Cooling Water (ICW) pump was inoperable for a period of time that was greater than allowed by TS. The licensee determined that the total OOS time for the 3B ICW pump was 4 days which exceeded the TS allowed outage time of 72 hours.
The LER documented that the 3B Intake Cooling Water (ICW) pump was inoperable for a period of time that was greater than allowed by TS. The licensee determined that the total OOS time for the 3B ICW pump was 4 days which exceeded the TS allowed outage time of 72 hours.


The inspectors reviewed the LER and the associated corrective action document (AR 1929130) to verify the accuracy and completene ss of the LER and the appropriateness of the licensee's corrective actions. The inspectors also reviewed the LER and AR to identify any licensee performance deficiencies associated with the issue.
The inspectors reviewed the LER and the associated corrective action document (AR 1929130) to verify the accuracy and completeness of the LER and the appropriateness of the licensees corrective actions. The inspectors also reviewed the LER and AR to identify any licensee performance deficiencies associated with the issue.


====b. Findings====
====b. Findings====
On September 28, 2013, while Unit 3 was in Mode 1, operators discovered that power to the 3B intake cooling water (ICW) pump breaker closing circuit and charging springs was lost. The under current (UC) fuse holder was noted to be slightly backed out and not firmly in place which resulted in the loss of breaker control power. Control power was restored after the fuse holder was pressed back in place on September 29, 2013.
On September 28, 2013, while Unit 3 was in Mode 1, operators discovered that power to the 3B intake cooling water (ICW) pump breaker closing circuit and charging springs was lost. The under current (UC) fuse holder was noted to be slightly backed out and not firmly in place which resulted in the loss of breaker control power. Control power was restored after the fuse holder was pressed back in place on September 29, 2013.


The licensee performed an investigation that determined that the 3B ICW pump had been inoperable for approximately four days (the time the pump was last started until the fuse holder was fully re-inserted), which was longer than the allowed TS 3.7.3, "Intake Cooling Water System," outage time of 72 hours. Although operators performed a daily verification that the breaker control power available white indicating light was lit on the breaker cubicle, the licensee determined that reasonable assurance could not be established that the fuses had enough contact with the base to ensure power to the closing spring even though the white control power light was lit. Therefore, the licensee concluded that the 3B ICW pump was inoperable for four days prior to discovery of the fuse holder condition. The inspectors determined the ICW system would have been able to perform its function even with the 3B ICW pump inoperable. The 3A and 3C ICW pumps were available and only one ICW pump is needed to remove design basis heat loads. Based on the availability of the ICW system to perform its heat removal function; and the relatively short duration of the condition prior to its discovery on September 28, the inspectors concluded that the event was of very low safety significance.
The licensee performed an investigation that determined that the 3B ICW pump had been inoperable for approximately four days (the time the pump was last started until the fuse holder was fully re-inserted), which was longer than the allowed TS 3.7.3, Intake Cooling Water System, outage time of 72 hours. Although operators performed a daily verification that the breaker control power available white indicating light was lit on the breaker cubicle, the licensee determined that reasonable assurance could not be established that the fuses had enough contact with the base to ensure power to the closing spring even though the white control power light was lit. Therefore, the licensee concluded that the 3B ICW pump was inoperable for four days prior to discovery of the fuse holder condition. The inspectors determined the ICW system would have been able to perform its function even with the 3B ICW pump inoperable. The 3A and 3C ICW pumps were available and only one ICW pump is needed to remove design basis heat loads. Based on the availability of the ICW system to perform its heat removal function; and the relatively short duration of the condition prior to its discovery on September 28, the inspectors concluded that the event was of very low safety significance.


The inspectors determined that a violation of TS limiting condition for operation (LCO) 3.7.3, "Intake Cooling Water System," occurred since Unit 3 was in Mode 1 and the 3B ICW pump was not returned to an operable status within 72 hours or the unit shut down and placed in hot standby within the next six hours. Although a violation of the TS LCO occurred, the violation was not attributable to an equipment failure that was avoidable by reasonable licensee quality assurance measures or management controls. The inspectors concluded that the violation would normally be characterized as Severity Level IV based on its very low safety significance. The NRC exercised enforcement discretion (Enforcement Action (EA)-14-058) in accordance with Section 2.2.4.d of the Enforcement Policy because the violation was not associated with a licensee performance deficiency; and therefore, it will not be considered in the assessment process or the NRC's Action Matrix. This issue is documented in the licensee's CAP as AR 1929130. Corrective actions included an investigation of the material condition of the fuse holder and base assembly, and a revision to the breaker operation procedure to include additional guidance on validating proper installation of the fuse holder when racking in a four kilovolt breaker. The LER is closed.
The inspectors determined that a violation of TS limiting condition for operation (LCO)3.7.3, Intake Cooling Water System, occurred since Unit 3 was in Mode 1 and the 3B ICW pump was not returned to an operable status within 72 hours or the unit shut down and placed in hot standby within the next six hours. Although a violation of the TS LCO occurred, the violation was not attributable to an equipment failure that was avoidable by reasonable licensee quality assurance measures or management controls. The inspectors concluded that the violation would normally be characterized as Severity Level IV based on its very low safety significance. The NRC exercised enforcement discretion (Enforcement Action (EA)-14-058) in accordance with Section 2.2.4.d of the Enforcement Policy because the violation was not associated with a licensee performance deficiency; and therefore, it will not be considered in the assessment process or the NRCs Action Matrix. This issue is documented in the licensees CAP as AR 1929130. Corrective actions included an investigation of the material condition of the fuse holder and base assembly, and a revision to the breaker operation procedure to include additional guidance on validating proper installation of the fuse holder when racking in a four kilovolt breaker. The LER is closed.


===.2 (Closed) LER 05000250/2013-008-00, Through-Wall Leak in 3A CCW Pump Threaded Fitting Caused Pump to be Inoperable Longer than Allowed Outage Time===
===.2 (Closed) LER 05000250/2013-008-00, Through-Wall Leak in 3A CCW Pump Threaded===
Fitting Caused Pump to be Inoperable Longer than Allowed Outage Time


====a. Inspection Scope====
====a. Inspection Scope====
The LER documented that the 3A component cooling water (CCW) pump was inoperable for a period of time that was greater than allowed by TS. The licensee determined that the total out of service time for the 3A CCW pump was 12 days which exceeded the TS allowed outage time of 72 hours.
The LER documented that the 3A component cooling water (CCW) pump was inoperable for a period of time that was greater than allowed by TS. The licensee determined that the total out of service time for the 3A CCW pump was 12 days which exceeded the TS allowed outage time of 72 hours.


The inspectors reviewed the LER and the associated corrective action documents (AR 1880602 and 1880576) to verify the accuracy and completeness of the LER and the appropriateness of the licensee's corrective actions. The inspectors also reviewed the LER and ARs to identify any licensee performance deficiencies associated with the issue.
The inspectors reviewed the LER and the associated corrective action documents (AR 1880602 and 1880576) to verify the accuracy and completeness of the LER and the appropriateness of the licensees corrective actions. The inspectors also reviewed the LER and ARs to identify any licensee performance deficiencies associated with the issue.


====b. Findings====
====b. Findings====
On June 7, 2013, Unit 3 was at 100 percent reactor power when the licensee identified a small leak of approximately 100 drops per minute at a threaded pipe connection on the 3A component cooling water pump casing. The licensee considered the pump to be operable because the leakage was within the make-up capacity of the CCW filling system. On June 19, the small leak had worsened to a steady stream of water and the pump was declared inoperable and taken out of service for repair. Upon removal and examination of the pipe, the licensee determined the pipe had a through-wall crack requiring replacement. The licensee's root cause analysis for the piping failure was documented in action request 1880602 and was previously reviewed by the inspectors.
On June 7, 2013, Unit 3 was at 100 percent reactor power when the licensee identified a small leak of approximately 100 drops per minute at a threaded pipe connection on the 3A component cooling water pump casing. The licensee considered the pump to be operable because the leakage was within the make-up capacity of the CCW filling system. On June 19, the small leak had worsened to a steady stream of water and the pump was declared inoperable and taken out of service for repair. Upon removal and examination of the pipe, the licensee determined the pipe had a through-wall crack requiring replacement. The licensees root cause analysis for the piping failure was documented in action request 1880602 and was previously reviewed by the inspectors.


The inspectors determined that the licensee had failed to identify and correct a flaw that resulted in through-wall pressure boundary leakage. The enforcement aspects of that issue were documented in NRC inspection report 2013003 (ADAMS accession number ML13211A151).
The inspectors determined that the licensee had failed to identify and correct a flaw that resulted in through-wall pressure boundary leakage. The enforcement aspects of that issue were documented in NRC inspection report 2013003 (ADAMS accession number ML13211A151).


Based on information gained from forensic examination of the failed pipe, the licensee determined that the pump would have been inoperable from the time the leak first became apparent on June 7, 2013. Although the pipe flaw size did not exceed acceptance criteria and the 3A CCW pump remained capable of performing its function, the licensee could not establish a reasonable degree of assurance that the flaw would not have increased in size during the mission time of the pump. TS limiting condition of operation (LCO) 3.7.2, "Component Cooling Water," requires three CCW pumps be operable in Modes 1 through 4, and with one inoperable pump, the two remaining pumps must be powered from independent power supplies within 72 hours or the unit shut down and placed in hot standby within six hours. Contrary to this requirement, the operable 3B and 3C CCW pumps were powered from the 3B safety related electrical bus for approximately 12 days with the 3A CCW pump in an inoperable condition. The inspectors utilized available risk-informed tools to assess the safety significance of the 3A CCW pump inoperability. Based on the availability of the 3B and 3C CCW pumps and the relatively short amount of time that the 3A CCW pump would have been considered inoperable, the inspectors concluded this event was of very low safety significance.
Based on information gained from forensic examination of the failed pipe, the licensee determined that the pump would have been inoperable from the time the leak first became apparent on June 7, 2013. Although the pipe flaw size did not exceed acceptance criteria and the 3A CCW pump remained capable of performing its function, the licensee could not establish a reasonable degree of assurance that the flaw would not have increased in size during the mission time of the pump. TS limiting condition of operation (LCO) 3.7.2, Component Cooling Water, requires three CCW pumps be operable in Modes 1 through 4, and with one inoperable pump, the two remaining pumps must be powered from independent power supplies within 72 hours or the unit shut down and placed in hot standby within six hours. Contrary to this requirement, the operable 3B and 3C CCW pumps were powered from the 3B safety related electrical bus for approximately 12 days with the 3A CCW pump in an inoperable condition. The inspectors utilized available risk-informed tools to assess the safety significance of the 3A CCW pump inoperability. Based on the availability of the 3B and 3C CCW pumps and the relatively short amount of time that the 3A CCW pump would have been considered inoperable, the inspectors concluded this event was of very low safety significance.


The inspectors determined in this case that there was no performance deficiency associated with the TS violation because the licensee monitored the leak for degradation and took action to declare the pump inoperable when it worsened. Additionally, the information obtained from forensic examination of the pipe flaw to assess the historical operability of the pump was not available to the licensee until after the condition had been repaired. The inspectors concluded that the violation would normally be characterized as Severity Level IV based on its very low safety significance. Although a violation of TS occurred, the violation was not attributable to an equipment failure that was avoidable by reasonable licensee qualit y assurance measures or management controls. The NRC exercised enforcement discretion (EA-14-058) in accordance with Section 2.2.4.d of the Enforcement Policy because the violation was not associated with a licensee performance deficiency. Therefore, it will not be considered in the assessment process or the NRC's Action Matr ix. This violation was documented in the licensee's CAP as AR 1883690. Licensee corrective actions included:
The inspectors determined in this case that there was no performance deficiency associated with the TS violation because the licensee monitored the leak for degradation and took action to declare the pump inoperable when it worsened. Additionally, the information obtained from forensic examination of the pipe flaw to assess the historical operability of the pump was not available to the licensee until after the condition had been repaired. The inspectors concluded that the violation would normally be characterized as Severity Level IV based on its very low safety significance. Although a violation of TS occurred, the violation was not attributable to an equipment failure that was avoidable by reasonable licensee quality assurance measures or management controls. The NRC exercised enforcement discretion (EA-14-058) in accordance with Section 2.2.4.d of the Enforcement Policy because the violation was not associated with a licensee performance deficiency. Therefore, it will not be considered in the assessment process or the NRCs Action Matrix. This violation was documented in the licensees CAP as AR 1883690. Licensee corrective actions included:
: (1) replacement of the leaking pipe on 3A CCW pump,
: (1) replacement of the leaking pipe on 3A CCW pump,
: (2) evaluations to replace similar CCW pump casing schedule 40 pipe nipples with schedule 80 and,
: (2) evaluations to replace similar CCW pump casing schedule 40 pipe nipples with schedule 80 and,
: (3) formal evaluations of existing leaks at threaded connections on Class 1, 2, and 3 systems to consider the potential for through-wall flaws. The LER is closed.
: (3) formal evaluations of existing leaks at threaded connections on Class 1, 2, and 3 systems to consider the potential for through-wall flaws. The LER is closed.


===.3 (Closed) LER 05000250/2014-001-00, Missed Surveillance Test Resulted in a Steam Generator Pressure Instrument Channel to be Inoperable Longer than Allowed Outage===
===.3 (Closed) LER 05000250/2014-001-00, Missed Surveillance Test Resulted in a Steam===
Generator Pressure Instrument Channel to be Inoperable Longer than Allowed Outage Time


Time  On January 3, 2014, Unit 3 was in Mode 1 at 100 percent reactor power when the instrument channel associated with Main Steam Line Pressure Transmitter PT-3-495 was found outside procedural acceptance criteria due to pressure transmitter (PT) drift. The surveillance for this instrument was considered a missed surveillance at the time of performance since it had not been completed for approximately 32 months and it had an 18-month TS requirement. The channel associated with PT-3-495 was considered inoperable from the time of replacement, January 3, 2014, back to the due date of the missed surveillance, March 9, 2013. PT-3-495 was replaced, calibrated successfully, and returned to service on January 4, 2014. The licensee determined the root cause of the event to be the deviation from the normal process of using a dedicated work order (WO) to satisfy surveillance requirements. Corrective actions included replacing PT-3-495, performing an extent of condition on all other work orders completed during the extended power uprate (EPU) outage to ensure TS compliance, and revising the surveillance tracking program procedure to verify that a surveillance test has been completed when crediting non-dedicated work orders. This event was associated with a violation of very low safety significance. The enforcement aspects associated with this LER are discussed in Section
On January 3, 2014, Unit 3 was in Mode 1 at 100 percent reactor power when the instrument channel associated with Main Steam Line Pressure Transmitter PT-3-495 was found outside procedural acceptance criteria due to pressure transmitter (PT) drift.
{{a|4OA2}}
 
==4OA2 of this report.==
The surveillance for this instrument was considered a missed surveillance at the time of performance since it had not been completed for approximately 32 months and it had an 18-month TS requirement. The channel associated with PT-3-495 was considered inoperable from the time of replacement, January 3, 2014, back to the due date of the missed surveillance, March 9, 2013. PT-3-495 was replaced, calibrated successfully, and returned to service on January 4, 2014. The licensee determined the root cause of the event to be the deviation from the normal process of using a dedicated work order (WO) to satisfy surveillance requirements. Corrective actions included replacing PT-3-495, performing an extent of condition on all other work orders completed during the extended power uprate (EPU) outage to ensure TS compliance, and revising the surveillance tracking program procedure to verify that a surveillance test has been completed when crediting non-dedicated work orders. This event was associated with a violation of very low safety significance. The enforcement aspects associated with this LER are discussed in Section 4OA2 of this report. The LER is closed.
The LER is closed.


{{a|4OA5}}
{{a|4OA5}}
==4OA5 Other Activities==
==4OA5 Other Activities==
 
===.1 (Closed) Temporary Instruction 2515/182 - Review of the Industry Initiative to Control===
===.1 (Closed) Temporary Instruction 2515/182 - Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks===
Degradation of Underground Piping and Tanks


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors conducted a review of records and procedures related to the licensee's program for buried piping and underground piping and tanks in accordance with Phase II of Temporary Instruction (TI) 2515-182 to confirm that the licensee's program contained attributes consistent with Sections 3.3.A and 3.3.B of Nuclear Energy Institute (NEI) 09-14, "Guideline for the Management of Buried Piping Integrity,"
The inspectors conducted a review of records and procedures related to the licensees program for buried piping and underground piping and tanks in accordance with Phase II of Temporary Instruction (TI) 2515-182 to confirm that the licensees program contained attributes consistent with Sections 3.3.A and 3.3.B of Nuclear Energy Institute (NEI) 09-14, Guideline for the Management of Buried Piping Integrity, Revision 3, and to confirm that these attributes were scheduled to be completed by the NEI 09-14, Revision 3, deadlines. The inspectors interviewed licensee staff responsible for the buried piping program and reviewed activities related to the buried piping program to determine if the program was managed in a manner consistent with the industrys buried piping initiative.
Revision 3, and to confirm that these attributes were scheduled to be completed by the NEI 09-14, Revision 3, deadlines. The inspectors interviewed licensee staff responsible for the buried piping program and reviewed activities related to the buried piping program to determine if the program was managed in a manner consistent with the industry's buried piping initiative.


The licensee's buried piping and underground piping and tanks program was inspected in accordance with paragraph 03.02.a of the TI and it was confirmed that activities which correspond to completion dates specified in the program which have passed since the Phase I inspection was conducted, have been completed. The licensee's buried piping and underground piping and tanks program was inspected in accordance with paragraph 03.02.b of the TI and responses to specific questions found in http://www.nrc.gov/reactors/operating/ops-experience/buried-pipe-ti-phase-2-insp-req-2011-11-16.pdf were submitted to the NRC headquarters staff.
The licensees buried piping and underground piping and tanks program was inspected in accordance with paragraph 03.02.a of the TI and it was confirmed that activities which correspond to completion dates specified in the program which have passed since the Phase I inspection was conducted, have been completed. The licensees buried piping and underground piping and tanks program was inspected in accordance with paragraph 03.02.b of the TI and responses to specific questions found in http://www.nrc.gov/reactors/operating/ops-experience/buried-pipe-ti-phase-2-insp-req-2011-11-16.pdf were submitted to the NRC headquarters staff.


====b. Findings====
====b. Findings====
Line 565: Line 568:


===.2 Cross-Cutting Aspect Cross-Reference===
===.2 Cross-Cutting Aspect Cross-Reference===
The table below provides a cross-reference from the 2013 third and fourth quarter findings and associated cross-cutting aspects to the new cross-cutting aspects resulting from the common language initiative. These aspects and any others identified since January 2014 will be evaluated for cross-cutting themes and potential substantive cross-cutting issues in accordance with Inspection Manual Chapter (IMC) 0305 starting with the 2014 mid-cycle assessment review.
Finding Old Cross-Cutting Aspect


The table below provides a cross-reference from the 2013 third and fourth quarter findings and associated cross-cutting aspects to the new cross-cutting aspects resulting from the common language initiative. These aspects and any others identified since January 2014 will be evaluated for cross-cutting themes and potential substantive cross-cutting issues in accordance with Inspection Manual Chapter (IMC) 0305 starting with the 2014 mid-cycle assessment review.
New Cross-Cutting Aspect


Finding Old Cross-Cutting Aspect New Cross-Cutting Aspect 05000250/2013004-01 H.2(c) H.7 05000250/2013004-02 H.4(c) H.2 05000250/2013004-03 H.3(a) H.5 05000251/2013004-04 H.4(b) H.8 05000250/2013004-05 H.2(c) H.7 05000251/2013005-01 H.3(a) H.5  
05000250/2013004-01 H.2(c)
H.7 05000250/2013004-02 H.4(c)
H.2 05000250/2013004-03 H.3(a)
H.5 05000251/2013004-04 H.4(b)
H.8 05000250/2013004-05 H.2(c)
H.7 05000251/2013005-01 H.3(a)
H.5  


{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings==
==4OA6 Meetings==
The resident inspectors presented the inspection results to Mr. Kiley and other members of licensee management on April 10, 2014. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information.
The resident inspectors presented the inspection results to Mr. Kiley and other members of licensee management on April 10, 2014. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information.


ATTACHMENT: SUPPPLEMENTAL INFORMATION KEY POINTS OF CONTACT Licensee Personnel
ATTACHMENT: SUPPPLEMENTAL INFORMATION KEY POINTS OF CONTACT  
: F. Banks, Quality Manager H. Benitez, PTN Engineering - Underground Piping Program Manager G. Bowen, EP staff C. Cashwell, Radiation Protection Manager T. Conboy, Plant General Manager P. Czaya, Licensing D. Dell, EP Staff C. Domingos, Engineering Director M. Downs, EP staff T. Eck, Security Manager K. Ellmers, Sr. Siren Technician M. Epstein, Emergency Preparedness Manager D. Funk, Operations Manager O. Hanek, Licensing Engineer M. Jones, System Engineering Manager M. Katz, Maintenance Manager M. Kiley, Site Vice-President  S. Mihalakea, Licensing D. Mothena, Emergency Preparedness Corporate Functional Area Manager N. Rios, Chemistry Manager D. Sluzka, Work Controls Manager B. Stamp, Training Manager R. Tomonto, Licensing Manager M. Wayland, Operations Director J. Wingate, EP staff


NRC Personnel
Licensee Personnel:
: C. Evans, Region II Legal Counsel and Enforcement Officer J. Hanna, Senior Risk Analyst, Division of Reactor Safety
F. Banks, Quality Manager H. Benitez, PTN Engineering - Underground Piping Program Manager G. Bowen, EP staff C. Cashwell, Radiation Protection Manager T. Conboy, Plant General Manager P. Czaya, Licensing D. Dell, EP Staff C. Domingos, Engineering Director M. Downs, EP staff T. Eck, Security Manager K. Ellmers, Sr. Siren Technician M. Epstein, Emergency Preparedness Manager D. Funk, Operations Manager O. Hanek, Licensing Engineer M. Jones, System Engineering Manager M. Katz, Maintenance Manager M. Kiley, Site Vice-President S. Mihalakea, Licensing D. Mothena, Emergency Preparedness Corporate Functional Area Manager N. Rios, Chemistry Manager D. Sluzka, Work Controls Manager B. Stamp, Training Manager R. Tomonto, Licensing Manager M. Wayland, Operations Director J. Wingate, EP staff


S. Sandal, Senior Project Engineer  
NRC Personnel:
C. Evans, Region II Legal Counsel and Enforcement Officer J. Hanna, Senior Risk Analyst, Division of Reactor Safety S. Sandal, Senior Project Engineer T. Su, Reactor Engineer  


T. Su, Reactor Engineer LIST OF ITEMS OPENED, CLOSED AND DISCUSSED
LIST OF ITEMS OPENED, CLOSED AND DISCUSSED  


Opened and Closed
Opened and Closed  


05000250/2014002-01  
05000250/2014002-01  


05000250/2014002-02 NCV
05000250/2014002-02 NCV  


NCV Failure to Take Adequate Corrective Actions to Correct Flow Induced Vibration Leads to CCW Piping Weld Failures. (Section 4OA2.2)  
NCV Failure to Take Adequate Corrective Actions to Correct Flow Induced Vibration Leads to CCW Piping Weld Failures.
 
(Section 4OA2.2)  


TS Channel Calibration of ESF Steam Line Protection Channel III Not Performed (Section 4OA2.3)
TS Channel Calibration of ESF Steam Line Protection Channel III Not Performed (Section 4OA2.3)
Closed 05000250/2013-009-00  
Closed  
 
05000250/2013-009-00  


05000250/2013-008-00  
05000250/2013-008-00  
Line 600: Line 616:
05000250/2014-001-00  
05000250/2014-001-00  


05000250, 251/2515/182 LER
05000250, 251/2515/182 LER  
 
LER 
 
LER 
 
TI Loose Breaker Control Power Fuse Holder Caused 3B ICW Pump to be Inoperable


Longer than Allowed Outage Time (Section
LER


4OA3.1)
LER
Through-Wall Leak in 3A CCW Pump Threaded Fitting Caused Pump to be Inoperable Longer than Allowed Outage


Time (Section 4OA3.2)  
TI Loose Breaker Control Power Fuse Holder Caused 3B ICW Pump to be Inoperable Longer than Allowed Outage Time (Section 4OA3.1)  


Missed Surveillance Test Resulted in a Steam Generator Pressure Instrument
Through-Wall Leak in 3A CCW Pump Threaded Fitting Caused Pump to be Inoperable Longer than Allowed Outage Time (Section 4OA3.2)


Channel to be Inoperable Longer than  
Missed Surveillance Test Resulted in a Steam Generator Pressure Instrument Channel to be Inoperable Longer than Allowed Outage Time (Section 4OA3.3)


Allowed Outage Time (Section 4OA3.3)  
Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks (Section 4OA5.1)  


Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks (Section 4OA5.1)
LIST OF  
LIST OF  


=DOCUMENTS REVIEWED=
=DOCUMENTS REVIEWED=


Action Requests:   01939933 01946565 01939548
Action Requests:  
01944754 01946589 01933839
 
01940963 01942544 01938704
01939933
01941033 01942618 01945528
01946565
01944767 01946385 01938123
01939548
01947210 01945663 01937543
01944754
01947219 01945746 01937722
01946589
01947489 01947747 01935879
01933839
01946040 01947063 01935975
01940963
01946270 01947139 01936028
01942544
01946324 01946076 01933286
01938704
01946524 01946078 01933231
01941033
01946660 01946217 01932528
01942618
01945718 01946225 01942421
01945528
01945773 01946303
01944767
01945968 01942398  
01946385
01938123
01947210
01945663
01937543
01947219
01945746
01937722
01947489
01947747
01935879
01946040
01947063
01935975
01946270
01947139
01936028
01946324
01946076
01933286
01946524
01946078
01933231
01946660
01946217
01932528
01945718
01946225
01942421
01945773
01946303
01945968
01942398  


Attachment
Section 1R04: Equipment Alignment
Section 1R04: Equipment Alignment
P&ID 5610-M-3075, Auxiliary Feedwater (AFW) System Turbine Drive for AFW Pumps
P&ID 5610-M-3075, Auxiliary Feedwater (AFW) System Turbine Drive for AFW Pumps Turkey Point System Description 117, Auxiliary Feedwater System P&ID 5613-M-3022, Emergency Diesel Engine and Oil System
Turkey Point System Description 117, Auxiliary Feedwater System
P&ID 5613-M-3022, Emergency Diesel Engine and Oil System
3-OP-023, Emergency Diesel Generator
3-OP-023, Emergency Diesel Generator
3-NOP-022, Emergency Diesel Generator Fuel Oil System
3-NOP-022, Emergency Diesel Generator Fuel Oil System
4-OSP-075.5, Auxiliary Feedwater System Flow Path Verification 3-OSP-075.5, Auxiliary Feedwater System Flow Path Verification P&ID 5613-M-3062, Safety Injection System
4-OSP-075.5, Auxiliary Feedwater System Flow Path Verification
Section 1R05: Fire Protection
3-OSP-075.5, Auxiliary Feedwater System Flow Path Verification
P&ID 5613-M-3062, Safety Injection System
Section 1R05: Fire Protection
0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions
0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions
Section 1R06: Flood Protection Measures
Section 1R06: Flood Protection Measures
Drawing 5610-C-1695, Network of Barriers for External Flood Protection 0-SMM-102.1, Flood Protection Stop Log and Penetration Seal Inspection  
Drawing 5610-C-1695, Network of Barriers for External Flood Protection
 
0-SMM-102.1, Flood Protection Stop Log and Penetration Seal Inspection
Section 1R15: Operability Evaluations
Section 1R15: Operability Evaluations
EN-AA-203-1001, Operability Determinations and Assessments 0-ADM-226, Operability Screening and Condition Reports
EN-AA-203-1001, Operability Determinations and Assessments
0-ADM-226, Operability Screening and Condition Reports
0-ADM-213, Technical Specification Related Equipment Out of Service Logbook
0-ADM-213, Technical Specification Related Equipment Out of Service Logbook
Section 1R18: Plant Modifications
Section 1R18: Plant Modifications
0-ADM-009, Containment Closeout Inspection
0-ADM-009, Containment Closeout Inspection
Section 1R19: Post Maintenance Testing
Section 1R19: Post Maintenance Testing
0-ADM-737, Post Maintenance Testing 4-SMI-059.08A, Power Range Nuclear Instrumentation Protection Channel N-4-41 Calibration 0-CMP-102.01, Troubleshooting and Repair Guidelines 0-CMI-059.10, Excore Neutron Detector Post Installation Inspection and Testing
0-ADM-737, Post Maintenance Testing
Section 1R20: Refueling and Other Outage Activities
4-SMI-059.08A, Power Range Nuclear Instrumentation Protection Channel N-4-41 Calibration
3-GOP-103, Power Operation to Hot Standby 3-GOP-305, Hot Standby to Cold Shutdown
0-CMP-102.01, Troubleshooting and Repair Guidelines
3-OSP-041.7, Reactor Coolant System Heatup and Cooldown
0-CMI-059.10, Excore Neutron Detector Post Installation Inspection and Testing
Temperature Verification 0-NOP-038.10, Manipulator Crane Operating Instruction 3-NOP-38.23, Fuel Transfer System Operations
Section 1R20: Refueling and Other Outage Activities
3-GOP-103, Power Operation to Hot Standby
3-GOP-305, Hot Standby to Cold Shutdown
3-OSP-041.7, Reactor Coolant System Heatup and Cooldown Temperature Verification
0-NOP-038.10, Manipulator Crane Operating Instruction
3-NOP-38.23, Fuel Transfer System Operations
3-NOP-040.02, Refueling Core Shuffle
3-NOP-040.02, Refueling Core Shuffle
0-ADM-035, Limitations and Precautions for Handling Fuel Assemblies
0-ADM-035, Limitations and Precautions for Handling Fuel Assemblies
MA-AA-101-1000, Foreign Material Exclusion Procedure 3-OP-038.1, Preparation of Refueling Activities
MA-AA-101-1000, Foreign Material Exclusion Procedure
Section 1EP2: Alert and Notification System Evaluation
3-OP-038.1, Preparation of Refueling Activities
Section 1EP2: Alert and Notification System Evaluation
Procedures and Reports
Procedures and Reports
Turkey Point Radiological Emergency Plan, Rev. 60 EP-SR-102-1000, Nuclear Division Florida Alert and Notification System Guideline, Rev. 8
Turkey Point Radiological Emergency Plan, Rev. 60
EP-SR-102-1000, Nuclear Division Florida Alert and Notification System Guideline, Rev. 8
Siren Maintenance Procedure No. 6.80.02, Rev. I  
Siren Maintenance Procedure No. 6.80.02, Rev. I  


Attachment WPS-4000 Series High Power Voice and Siren System Operating and Troubleshooting Manual PI-AA-204, Condition Identification and Screening Process, Rev. 22 PI-AA-205, Condition Evaluation and Corrective Actions, Rev. 23  
WPS-4000 Series High Power Voice and Siren System Operating and Troubleshooting Manual
 
PI-AA-204, Condition Identification and Screening Process, Rev. 22
PI-AA-205, Condition Evaluation and Corrective Actions, Rev. 23
Records and Data
Records and Data
Documentation of Quarterly siren maintenance for 2012 and 2013
Documentation of Quarterly siren maintenance for 2012 and 2013
Line 682: Line 734:
1899615; Siren S-12 Lightning damage
1899615; Siren S-12 Lightning damage
1889287; Siren S-38 loss of communications
1889287; Siren S-38 loss of communications
1886797; Siren S-28 pole damage 1935265; 2012 annual maintenance data hard drive failure
1886797; Siren S-28 pole damage
1935265; 2012 annual maintenance data hard drive failure
1935171; Admin errors on ANS documentation
1935171; Admin errors on ANS documentation
Section 1EP3: Emergency Preparedness Organization Staffing and Augmentation System Procedures
Section 1EP3: Emergency Preparedness Organization Staffing and Augmentation
System
Procedures
EPLAN, Turkey Point Plant Radiological Emergency Plan, Rev. 60
EPLAN, Turkey Point Plant Radiological Emergency Plan, Rev. 60
EP-AA-100-1000-1007, Conducting EP Regulatory Reviews, Rev. 1
EP-AA-100-1000-1007, Conducting EP Regulatory Reviews, Rev. 1
0-EPIP-20101, "10CFR50.54(q) Screen and Evaluation (ARs: 1892310, Rev. 1, 1901378, and
0-EPIP-20101, 10CFR50.54(q) Screen and Evaluation (ARs: 1892310, Rev. 1, 1901378, and
1892294) EP-AD-006, Maintaining the Emergency Response Directory (ERD) & Requirements for Manual Callout Surveillance, Rev. 14 EP-AD-011, "Instructions for Maintaining the Emergency Preparedness NRC Performance Indicators" EP-AD-012, Autodialer Maintenance and Testing Instructions, Rev. 7 EP-AD-015, Emergency Preparedness ERO Staffing Advisory Committee and Training Committee, Rev. 14 EP-AA-01, Emergency Preparedness Expectations, Rev. 0  
1892294)
 
EP-AD-006, Maintaining the Emergency Response Directory (ERD) & Requirements for Manual
Callout Surveillance, Rev. 14
EP-AD-011, Instructions for Maintaining the Emergency Preparedness NRC Performance
Indicators
EP-AD-012, Autodialer Maintenance and Testing Instructions, Rev. 7
EP-AD-015, Emergency Preparedness ERO Staffing Advisory Committee and Training
Committee, Rev. 14
EP-AA-01, Emergency Preparedness Expectations, Rev. 0
Records and Data
Records and Data
2013 and 2014 ERO Team Staff Assignments 2013 off-hour augmentation test reports Auto-dialer records: 1/8/2014 - 1/22/2014  
2013 and 2014 ERO Team Staff Assignments
 
2013 off-hour augmentation test reports
Auto-dialer records: 1/8/2014 - 1/22/2014
Corrective Action Documents
Corrective Action Documents
1746619; EOF ST/CO Comm. potential to drop below 3
1746619; EOF ST/CO Comm. potential to drop below 3
1746623; EOF Fuels Eng.
1746623; EOF Fuels Eng. potential to drop below 3
potential to drop below 3 1746630; OSC Dose Recorder potential to drop below 3
1746630; OSC Dose Recorder potential to drop below 3
1746635; OSC Doc. Control potential to drop below 3
1746635; OSC Doc. Control potential to drop below 3
1746638; Duty Call Supervisor potential to drop below 3
1746638; Duty Call Supervisor potential to drop below 3
1746644; EOF RP Manager potential to drop below 3
1746644; EOF RP Manager potential to drop below 3
1801659; EOF Recovery Manager potential to drop below 3 1898914; EOF RP Manager dropped below 3
1801659; EOF Recovery Manager potential to drop below 3
1898914; EOF RP Manager dropped below 3  


Attachment Section 1EP4: Emergency Action Level and Emergency Plan Changes
Section 1EP4: Emergency Action Level and Emergency Plan Changes
Procedures
Procedures
Emergency Plan, Rev. 60 0-EPIP-20101, 10CFR50.54(q) Screen and Evaluation, Rev. 1
Emergency Plan, Rev. 60
0-EPIP-20101, 10CFR50.54(q) Screen and Evaluation, Rev. 1
Change Packages
Change Packages
0-HPS-090, Inventory of Radiation Protection Emergency Equipment, Rev. 2 0-EPIP-20132, "Technical Support Center (TSC) Activation and Operation," Rev. 7
0-HPS-090, Inventory of Radiation Protection Emergency Equipment, Rev. 2
0-EPIP-20132, Technical Support Center (TSC) Activation and Operation, Rev. 7
Corrective Action Documents
Corrective Action Documents
1935172; RCS sampling procedure has no high rad precautions/limitation statements 1908087; Editorial Change to Emergency Coordinator Duties 1908448; Excessive RCS Activity word deletion 1927976; Actions if Plant Site Inaccessible
1935172; RCS sampling procedure has no high rad precautions/limitation statements
Section 1EP5: Maintenance of Emergency Preparedness
1908087; Editorial Change to Emergency Coordinator Duties
1908448; Excessive RCS Activity word deletion
27976; Actions if Plant Site Inaccessible
Section 1EP5: Maintenance of Emergency Preparedness
Procedures
Procedures
EP-AA-100-1001, Guidelines for Maintaining Emergency Preparedness, Rev. 5
EP-AA-100-1001, Guidelines for Maintaining Emergency Preparedness, Rev. 5
0-EPIP-20126, Off-Site Dose Calculations - Extended Power Uprate, Rev.7 0-NCZP-041.1, Obtaining a Reactor Coolant Sample, Rev. 1 EP-AA-105-1000, Equipment Important to Emergency Response, Rev. 0
0-EPIP-20126, Off-Site Dose Calculations - Extended Power Uprate, Rev.7
0-EPIP-20101, Duties of the Emergency Coordinator, Rev. 14  
0-NCZP-041.1, Obtaining a Reactor Coolant Sample, Rev. 1
 
EP-AA-105-1000, Equipment Important to Emergency Response, Rev. 0
0-EPIP-20101, Duties of the Emergency Coordinator, Rev. 14
Records and Data
Records and Data
Turkey Point 2014 Emergency Planning public brochure PTN-12-010, Turkey Point Nuclear Oversight Report
Turkey Point 2014 Emergency Planning public brochure
PTN-12-010, Turkey Point Nuclear Oversight Report
PTN-13-009, Turkey Point Nuclear Oversight Report
PTN-13-009, Turkey Point Nuclear Oversight Report
AT-01.16, Single AR Report for DEP Opportunity Evaluation for NOUE Declared on 4/2/12
AT-01.16, Single AR Report for DEP Opportunity Evaluation for NOUE Declared on 4/2/12
AT-01.16, Single AR Report for Unit 4 Reactor Trip
AT-01.16, Single AR Report for Unit 4 Reactor Trip
AT-01.16, Single AR Report for Critique of Notifications during Unusual Event on 4/19/13 2012 10/25 Drill report
AT-01.16, Single AR Report for Critique of Notifications during Unusual Event on 4/19/13
2012 10/25 Drill report
2013 August Drill Report
2013 August Drill Report
2013 December Drill Report
2013 December Drill Report
Line 728: Line 800:
1750814; DEP opportunity had different results than lesson package
1750814; DEP opportunity had different results than lesson package
1751998; DEP opportunity evaluation for NOUE declared at PTN on 4/2/12
1751998; DEP opportunity evaluation for NOUE declared at PTN on 4/2/12
1761448; TSC backup power did not function during loss of normal power 1772978; Concrete ramps located where flood stop logs get installed 1817868; General rollup during EP drill
1761448; TSC backup power did not function during loss of normal power
1772978; Concrete ramps located where flood stop logs get installed
1817868; General rollup during EP drill
1867707; Unit 4 Unusual Event - 4/19/13
1867707; Unit 4 Unusual Event - 4/19/13
1869299; Critique of notifications during Unusual Event on 4/19/13
1869299; Critique of notifications during Unusual Event on 4/19/13
1876973; EP indicator dropped below green
1876973; EP indicator dropped below green
1883638; Dual roles for ERO responders
1883638; Dual roles for ERO responders  
Attachment 1884141; EP NRC inspection observations 1891427; EP DEP indicator showing a declining trend in EOF/TSC 1934762; Review E-Plan 5.1.2 regarding post-accident sampling
 
Section 4OA1: Performance Indicator Verification
1884141; EP NRC inspection observations
1891427; EP DEP indicator showing a declining trend in EOF/TSC
1934762; Review E-Plan 5.1.2 regarding post-accident sampling
Section 4OA1: Performance Indicator Verification
Procedures
Procedures
0-ADM-032, NRC Performance Indicators Turkey Point, Rev. 5
0-ADM-032, NRC Performance Indicators Turkey Point, Rev. 5
Line 740: Line 817:
Documentation of DEP opportunities for 2nd -3rd quarter 2013
Documentation of DEP opportunities for 2nd -3rd quarter 2013
Documentation of ANS tests for 2nd quarter - 3th quarter 2013
Documentation of ANS tests for 2nd quarter - 3th quarter 2013
Documentation of drill and exercise participation for 2nd quarter - 3rd quarter 2013 Various ERO Personnel Qualification and Participation records
Documentation of drill and exercise participation for 2nd quarter - 3rd quarter 2013
Various ERO Personnel Qualification and Participation records
Corrective Action Documents
Corrective Action Documents
1682047, EP self-assessment - NRC drill participation performance indicator improvement
1682047, EP self-assessment - NRC drill participation performance indicator improvement
570387, Drill and exercise participation affecting NRC PI 472365, Seven SROs had not participated in a qualified opportunity in 8 quarters
570387, Drill and exercise participation affecting NRC PI
Section 4OA5: Other Activities
2365, Seven SROs had not participated in a qualified opportunity in 8 quarters
Section 4OA5: Other Activities
Procedures
Procedures
ER-AA-102, Underground Piping and Tanks Integrity Program, Rev. 6
ER-AA-102, Underground Piping and Tanks Integrity Program, Rev. 6
ER-AA-102-1000, Underground Piping and Tanks Integrity Examination Procedure, Rev. 2
ER-AA-102-1000, Underground Piping and Tanks Integrity Examination Procedure, Rev. 2
Corrective Action Program Documents
Corrective Action Program Documents
AR 1678662, Generated to Track Actions Associated with Meeting Milestones of NEI 09-14, Rev. 3 AR 01802204, QHSA for NRC Buried Piping Inspection (TI 2515/182) AR 1915405, QHSA for NRC Buried Piping Inspection (TI 2515/182 Phase 2) AR 1915405-01, PTN Response to Enclosure 2 "TI-182 Phase 2 Questions"
AR 1678662, Generated to Track Actions Associated with Meeting Milestones of NEI 09-14,
 
Rev. 3
AR 01802204, QHSA for NRC Buried Piping Inspection (TI 2515/182)
AR 1915405, QHSA for NRC Buried Piping Inspection (TI 2515/182 Phase 2)
AR 1915405-01, PTN Response to Enclosure 2 TI-182 Phase 2 Questions
Other Documents
Other Documents
Buried Piping Program Health Report (7/1/2013 - 9/30/2013)
Buried Piping Program Health Report (7/1/2013 - 9/30/2013)
Drawing 5610-C13, Utility Piping - Main Plant Area, Rev. 27
Drawing 5610-C13, Utility Piping - Main Plant Area, Rev. 27
PTN Buried Piping Program Basis Document, Revision 1 Turkey Point Nuclear Station Underground Piping and Tanks Condition Assessment Plan, Rev. 2 Unit 3 Circulating Water Pipe NDE Inspection, Turkey Point Nuclear Station, by Pure Technologies, US, August 2012
PTN Buried Piping Program Basis Document, Revision 1
Turkey Point Nuclear Station Underground Piping and Tanks Condition Assessment
Plan, Rev. 2
Unit 3 Circulating Water Pipe NDE Inspection, Turkey Point Nuclear Station, by Pure
Technologies, US, August 2012  


LIST OF ACRONYMS
LIST OF ACRONYMS
AR   Action Request CAP Corrective Action Program
AR
CCW Component Cooling Water
Action Request
CFR Code of Federal Regulations
CAP
EAL   Emergency Action Level
Corrective Action Program
EDG   Emergency Diesel Generator IST   Inservice Testing NAP   Nuclear Administrative Procedure
CCW
NRC   Nuclear Regulatory Commission
Component Cooling Water
PI   Performance Indicator
CFR
P&ID   Piping and Instrumentation Drawing RCE   Root Cause Evaluation RCP   Reactor Coolant Pump
Code of Federal Regulations
RCS   Reactor Coolant System
EAL  
TS   Technical Specifications
 
U3   Unit 3 U4   Unit 4 UFSAR Updated Final Safety Analysis Report
Emergency Action Level
WO   Work Order
EDG  
GOP   General Operating Procedure
 
ONOP   Off Normal Operating Procedure
Emergency Diesel Generator
IST  
 
Inservice Testing
NAP  
 
Nuclear Administrative Procedure
NRC
Nuclear Regulatory Commission
PI  
 
Performance Indicator
P&ID
Piping and Instrumentation Drawing
RCE  
 
Root Cause Evaluation
RCP  
 
Reactor Coolant Pump
RCS  
 
Reactor Coolant System
TS  
 
Technical Specifications
U3
Unit 3
U4
Unit 4
UFSAR
Updated Final Safety Analysis Report
WO  
 
Work Order
GOP
General Operating Procedure
ONOP
Off Normal Operating Procedure
}}
}}

Latest revision as of 21:18, 10 January 2025

IR 05000250-14-002, 05000251-14-002; on 01/01/2014 - 3/31/2014; Turkey Point Nuclear Plant, Units 3 & 4; Problem Identification and Resolution
ML14121A165
Person / Time
Site: Turkey Point  NextEra Energy icon.png
Issue date: 04/30/2014
From: Croteau R
Division Reactor Projects II
To: Nazar M
Florida Power & Light Co
References
EA-14-058 IR-14-002
Download: ML14121A165 (35)


Text

April 30, 2014

SUBJECT:

TURKEY POINT NUCLEAR GENERATING STATION - NRC INTEGRATED INSPECTION REPORT 05000250/2014002, 05000251/2014002 AND EXERCISE OF ENFORCEMENT DISCRETION

Dear Mr. Nazar:

On March 31, 2014, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Turkey Point Nuclear Generating Station Units 3 and 4. On April 10, 2014, the NRC inspectors discussed the results of the inspection with Mr. Kiley and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

The findings involved violations of NRC requirements. The NRC is treating these violations as non-cited (NCVs) consistent with Section 2.3.2.a of the Enforcement Policy.

In addition, the NRC is exercising enforcement discretion for two violations of very low safety significance that were not the result of performance deficiencies. Contrary to Technical Specification (TS) 3.7.3, Intake Cooling Water System, Unit 3 operated in Mode 1 with the 3B intake cooling water pump inoperable for longer than the TS allowed outage time due to a loose fuse holder. Contrary to TS 3.7.2, Component Cooling Water System, Unit 3 operated in Mode 1 with the 3A component cooling water pump inoperable for longer than the TS allowed outage time due to leakage from the pump casing vent. Although violations of the TS occurred, the violations were not attributable to equipment failures that were avoidable by reasonable licensee quality assurance measures or management controls. Therefore, the TS 3.7.3 and 3.7.2 violations were not associated with licensee performance deficiencies. The NRC concluded that the violations were of very low safety significance. Based on these facts, I have been authorized, after consultation with the Director, Office of Enforcement, and the Regional Administrator, to exercise enforcement discretion in accordance with Section 2.2.4.d of the Enforcement Policy and refrain from issuing enforcement for the violations. These violations will not be considered in the assessment process or the NRCs Action Matrix. If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator Region II; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington DC 20555-0001; and the NRC Resident Inspector at Turkey Point Nuclear Generating Station Units 3 and 4.

If you disagree with a cross-cutting aspect assignment or the finding not associated with a regulatory requirement in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II; and the NRC resident inspector at the Turkey Point Nuclear Generating Station Units 3 and 4.

Additionally, as we informed you in the most recent NRC integrated inspection report, cross-cutting aspects identified in the last six months of 2013 using the previous terminology were being converted in accordance with the cross-reference in Inspection Manual Chapter 0310.

Section 4OA5 of the enclosed report documents the conversion of these cross-cutting aspects which will be evaluated for cross-cutting themes and potential substantive cross-cutting issues in accordance with IMC 0305 starting with the 2014 mid-cycle assessment review. If you disagree with the cross cutting aspect assigned, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region II; and the NRC Resident Inspector at the Turkey Point Nuclear Generating Station.

In accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding, of the NRCs Rules of Practice, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRCs Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/William Jones RA for/

Richard P. Croteau, Director

Division of Reactor Projects

Docket Nos.: 50-250, 50-251 License Nos.: DPR-31, DPR-41

Enclosure:

Inspection Report 05000250/2014002, 05000251/2014002,

w/Attachment: Supplemental Information

REGION II==

Docket Nos:

50-250, 50-251

License Nos:

DPR-31, DPR-41

Report Nos:

05000250/2014002, 05000251/2014002

Licensee:

Florida Power & Light Company (FP&L)

Facility:

Turkey Point Nuclear Generating Station, Units 3 & 4

Location:

9760 S. W. 344th Street Homestead, FL 33035

Dates:

January 1 to March 31, 2014

Inspectors:

T. Hoeg, Senior Resident Inspector

M. Endress, Resident Inspector

M. Speck, Senior Emergency Preparedness Inspector (1EP2-5, 4OA1)

S. Sanchez, Senior Emergency Preparedness Inspector (1EP2-5, 4OA1)

C. Fontana, Emergency Preparedness Inspector (1EP2-5, 4OA1)

R. Carrion, Senior Reactor Inspector (4OA5)

Approved by:

Daniel W. Rich, Chief

Reactor Projects Branch 3

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000250/2014002, 05000251/2014002; 01/01/2014 - 3/31/2014; Turkey Point Nuclear

Plant, Units 3 & 4; Problem Identification and Resolution.

The report covered a three-month period of inspection by the resident inspectors and region-based specialist inspectors. Two Green non-cited violations were identified. The significance of inspection findings are indicated by their color (i.e., Green, White, Yellow, or Red) and determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process, (SDP) dated June 2, 2011. The cross-cutting aspects were determined using IMC 0310,

Components Within the Cross-Cutting Areas, dated December 19, 2013. All violations of NRC requirements were dispositioned in accordance with the NRCs Enforcement Policy dated July 9, 2013. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Corrective Action, was identified when the licensee failed to implement corrective actions that addressed the low stress high cycle fatigue of component cooling water (CCW) relief valve (RV) 4-747B piping caused by flow induced vibration. As a result, CCW system flow induced vibration resulted in weld cracks and system pressure boundary leakage in January 2014. This issue was placed in the licensees corrective action program (CAP) as action request (AR) 1931761. Corrective actions included performing a root cause evaluation, implementing special instructions to minimize the time that split header operation is performed, and developing a plan to replace the existing relief valve with an orifice or alternate relief valve.

The performance deficiency was more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to implement adequate corrective actions to address CCW system flow induced vibration resulted in weld cracks and CCW system pressure boundary leakage in January 2014. The finding was screened using Exhibit 1, Mitigating Systems Screening Questions, found in Inspection Manual Chapter 0609, Significance Determination Process, Appendix A,

Significance Determination Process (SDP) for Findings At-Power (June 19, 2012). The inspectors determined the finding was of very low safety significance (Green) because the finding did not affect design or qualification, did not represent a loss of system function, and did not represent an actual loss of function of a TS train of equipment. The finding was associated with a cross-cutting aspect in the evaluation component of the problem identification and resolution area because the licensee did not thoroughly evaluate issues and corrective actions from previous weld failures on CCW system RV-4-747B piping caused by flow induced vibration (P.2). (Section 4OA2.2)

  • Green: A self-revealing non-cited violation (NCV) of TS Section 3.3.2, Engineered Safety Features Actuation Instrumentation, (ESF) was identified when the licensee failed to perform the channel calibration of Unit 3 ESF steam pressure protection channel III within the required 18-month frequency which resulted in operation with steam generator pressure transmitter PT-3-495 inoperable for approximately 10 months. This issue was placed in the licensees CAP as AR 1938191. Corrective actions included replacing PT-3-495, performing an extent of condition on all other work orders completed during the extended power uprate (EPU) outage to ensure TS compliance, and revising the surveillance tracking program procedure to require verification that the required surveillance testing is completed prior to crediting non-dedicated work orders.

The performance deficiency was more than minor because it was associated with the human performance attribute of the mitigating systems cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to perform the channel calibration surveillance test procedure for transmitter PT-3-495 within the 18-month required frequency resulted in 10 months of channel inoperability. The finding was screened using Exhibit 1, Mitigating Systems Screening Questions, found in Inspection Manual Chapter 0609, Significance Determination Process, Appendix A, Significance Determination Process for Findings At-Power (June 19, 2012). The inspectors determined the finding was of very low safety significance (Green) because the finding did not affect design or qualification, did not represent a loss of system function, and did not represent an actual loss of function of a technical specification train of equipment. The finding was associated with a cross-cutting aspect in the work management component of the human performance area because the licensee failed to implement their process for planning, controlling, and executing required surveillance tests (H.5). (Section 4OA2.3)

Licensee Identified Violations

None

REPORT DETAILS

Summary of Plant Status

Unit 3 began this inspection period at 100 percent of rated thermal power (RTP) where it remained until March 17 when it was shut down for a planned refueling outage that continued through the end of this inspection period.

Unit 4 began this inspection period at 100 percent of RTP where it remained throughout this inspection period.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity (R)

==1R04 Equipment Alignment

==

.1 Partial Equipment Walk Downs (Quarterly)

a. Inspection Scope

The inspectors conducted three partial alignment verifications of the safety-related systems listed below. These inspections included reviews using plant lineup procedures, operating procedures, and piping and instrumentation drawings, which were compared with observed equipment configurations to verify that the critical portions of the systems were correctly aligned to support operability. The inspectors also verified that the licensee had identified and resolved equipment alignment problems that could cause initiating events or impact the capability of mitigating systems or barriers by entering them into the CAP. Documents reviewed are listed in the Attachment.

  • 3B High Head Safety Injection (HHSI) while the 3A HHSI was OOS

b. Findings

No findings were identified.

.2 Equipment Alignment (Semi-annual)

a. Inspection Scope

The inspectors conducted a detailed review of the alignment and material condition of the A standby feed water system train to verify its capability to meet its design basis function while the B standby feed water system was OOS for troubleshooting and repair.

The inspectors utilized licensee procedure 0-OSP-074.3, Standby Steam Generator Feedwater Pumps Availability and Drawings 5610-M-3074, Feedwater System, Sheets 1 and 2, to verify the system alignment was correct. During the walkdown, the inspectors verified, as appropriate, that: 1) valves were correctly positioned and did not exhibit leakage that would impact their function, 2) electrical power was available as required, 3) major portions of the system and components were correctly labeled, cooled, and ventilated, 4) hangers and supports were correctly installed and functional, 5) essential support systems were operational, 6) ancillary equipment or debris did not interfere with system performance, 7) tagging clearances were appropriate, and 8)valves were locked as required by the licensees locked valve program. Other items reviewed included the operator workaround list, the temporary modification list, system health reports, system description, and open maintenance work orders. In addition, the inspectors reviewed the licensees CAP to ensure that the licensee was identifying and resolving associated equipment problems.

b. Findings

No findings were identified.

==1R05 Fire Protection

==

.1 Fire Area Walk downs

a. Inspection Scope

The inspectors toured the following five plant areas to evaluate conditions related to control of transient combustibles, ignition sources, material condition, and operational status of fire protection systems including fire barriers used to prevent fire damage and propagation. The inspectors reviewed these activities using provisions in the licensees procedure 0-ADM-016, Fire Protection Plan and 10 CFR Part 50, Appendix R. The licensees fire impairment lists were routinely reviewed. In addition, the inspectors reviewed the condition report database to verify that fire protection problems were being identified and appropriately resolved. The inspectors accompanied fire watch roving personnel on a tour of fire protection impairments and risk significant fire areas to assure monitoring of area status and to verify proper identification and handling of transient combustibles. The following areas were inspected:

  • DC Equipment Room 4B Fire Zone 101
  • DC Equipment Room 3A Fire Zone 104
  • 3B EDG Fuel Oil Day Tank Room Fire Zone 74
  • Auxiliary Building Electrical Equipment Room Fire Zone 25
  • 3B 4kV Switchgear Room Fire Zone 70

b. Findings

No findings were identified.

==1R07 Heat Sink Performance

a. Inspection Scope

==

The inspectors selected the 3A component cooling water heat exchanger to verify the licensee was performing periodic cleaning and inspections to ensure its tubes remained clear and unobstructed. The inspectors observed portions of the heat exchanger cleaning and inspection performed by the licensee under WO 40295368. The inspectors verified the cleaning and inspection was performed and properly documented in accordance with completed maintenance procedure 0-PMM-030.01, Component Cooling Water Heat Exchanger Cleaning and Inspection. The inspectors also reviewed completed licensee procedure 3-OSP-019.4, Component Cooling Water Heat Exchanger Performance Monitoring to ensure the heat exchanger was restored, leak tested, and returned to service with no deficiencies.

b. Findings

No findings were identified.

==1R11 Licensed Operator Requalification Program

Resident Inspector Quarterly Review

==

.1 Simulator Observations

a. Inspection Scope

The inspectors performed the following two inspection samples of simulator observations and assessed licensed operator performance while training. These observations included procedural use and adherence, response to alarms, communications, command and control, and coordination and control of the reactor plant operations.

On February 6, 2014, the inspectors assessed licensed operator performance in the plant-specific simulator during an emergency preparedness drill scenario. The training scenario was started with the unit at 100 percent power and steady state conditions.

Event simulations consisted of damage to an irradiated fuel assembly in the spent fuel pit, a large break loss of coolant accident (LOCA), and anticipated transient without scram (ATWS). Operators responded to the simulation using off-normal procedures 3-ONOP-067, Radioactive Effluent Release, and 3-ONOP-041.4, Excessive Reactor Coolant System Activity. Emergency procedures used by the crew to safely mitigate the events included 3-EOP-E-0, Reactor Trip and 3-EOP-FR-S-1, Response to Nuclear Power Generation ATWS. The inspectors specifically checked that the simulated emergency classifications of Alert and General Emergency were done in accordance with licensee procedure, 0-EPIP-20101, Duties of the Emergency Coordinator.

On March 12, 2014, the inspectors observed and assessed operator training associated with an upcoming refueling outage on Unit 3 scheduled for March 17, 2014. The licensed operators participated in just in time training for collapsing a pressurizer bubble and transition to solid pressure control in accordance with procedure 3-NOP-041.02, Pressurizer Operation.

During these simulator observations, the simulator board configurations were compared with actual plant control board configurations concerning recent power up rate modifications. The inspectors specifically evaluated the following attributes related to operating crew performance and the licensee evaluation:

  • Clarity and formality of communication
  • Ability to take timely action to safely control the unit
  • Prioritization, interpretation, and verification of alarms
  • Correct use and implementation of off-normal and emergency operating procedures and emergency plan implementing procedures
  • Control board operation and manipulation, including high-risk operator actions
  • Oversight and direction provided by shift supervisor, including ability to identify and implement appropriate TS actions and emergency plan classification and notification
  • Crew overall performance and interactions
  • Evaluators control of the scenario and post scenario evaluation of crew performance

b. Findings

No findings were identified.

.2 Control Room Observations

a. Inspection Scope

The inspectors performed the following focused control room observations and assessed licensed operator performance in the control room. These observations included daily routine surveillance testing, response to alarms, communications, shift turnovers, and coordination of plant activities. These observations were conducted to verify operator compliance with station operating guidelines, such as use of procedures, control and manipulation of components, and communications. On March 5, 2014, the inspectors did a focused observation on Unit 4 consisting of a reactor coolant system primary water dilution per 0-OP-046, Enclosure 6, Chemical Volume Control System Boron Concentration Control. Specifically, the inspectors observed the reactor operators performing the pre-job brief per 0-ADM-200, Attachment 7, Planned Reactivity Manipulations for Maintaining Steady State Plant Conditions and verified the operators complied with the applicable procedure during the evolution.

The inspectors focused on the following conduct of operations attributes as

appropriate:

  • Operator compliance and use of procedures
  • Control board manipulations
  • Communication between crew members
  • Use and interpretation of plant instruments, indications and alarms
  • Use of human error prevention techniques
  • Documentation of activities, including initials and sign-offs in procedures
  • Supervision of activities, including risk and reactivity management

b. Findings

No findings were identified.

==1R12 Maintenance Effectiveness

a. Inspection Scope

==

The inspectors reviewed known equipment problems associated with the 4C component cooling water pump and the R-4-11 containment radiation monitor affecting the maintenance rule program and equipment performance history trends associated with the equipment. The inspectors reviewed the licensees activities to meet the requirements of 10 CFR 50.65, Requirements for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, and licensee procedure NAP-415, Maintenance Rule Program Administration. The inspectors focused on maintenance rule scoping, characterization of maintenance problems and failed components, risk significance, determination of a(1) or a(2) performance criteria classification, corrective actions, and the appropriateness of established performance goals and monitoring criteria. The inspectors also interviewed responsible engineers and observed or reviewed corrective maintenance activities. The inspectors verified that equipment problems were being identified and appropriately entered into the licensees CAP. The inspectors used the licensee maintenance rule data base, system health reports, maintenance rule unavailability status reports, and the CAP as sources of information on tracking and resolution of issues.

  • 4C Component Cooling Water Pump Unavailability, AR 01942801
  • R-4-11 Containment Radiation Monitor Unavailability, AR 01946565

b. Findings

No findings were identified.

==1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

==

The inspectors completed in-office reviews and control room inspections of the licensees risk assessment of four emergent or planned maintenance activities. The inspectors verified the licensees risk assessment and risk management activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and procedures 0-ADM-068, Work Week Management; WM-AA-1000, Work Activity Risk Management; and O-ADM-225, On Line Risk Assessment and Management. The inspectors also reviewed the effectiveness of the licensees contingency actions to mitigate increased risk resulting from the degraded equipment and the licensee assessment of aggregate risk using procedure OP-AA-104-1007, Online Aggregate Risk. The inspectors discussed the on-line risk monitor (OLRM) results with the control room operators and verified all applicable out of service equipment was included in the OLRM calculation. The inspectors evaluated the following four risk assessments during the inspection period:

  • 3A Component Cooling Water (CCW) Heat Exchanger, 3B CCW Pump, and 3C Coolant Charging Pump OOS

b. Findings

No findings were identified.

==1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

==

The inspectors evaluated the technical adequacy of licensee evaluations to ensure that TS operability was properly justified and the subject component or system remained available such that no unrecognized increase in risk occurred for the five operability evaluations described in the ARs listed below. The inspectors reviewed applicable sections of the UFSAR to determine if the system or component remained available to perform its intended function. In addition, when applicable, the inspectors reviewed compensatory measures implemented to verify that the affected equipment remained capable of performing its design function. The inspectors also reviewed a sampling of condition reports to verify that the licensee was routinely identifying and correcting any deficiencies associated with operability evaluations.

  • AR 1931750, Missed Technical Specification Surveillances
  • AR 1940683, Uncertainty Calculation for BAST Level
  • AR 1930745, PT-3-495 Found Out of Calibration During 3-SMI-072.2

b. Findings

No findings were identified.

==1R18 Plant Modifications

Temporary Plant Modifications

a. Inspection Scope

==

The inspectors reviewed a temporary plant modification technical evaluation for leaving a robot in the containment building 14 foot elevation while at full power. The robot became stuck when one of its tracks became dislodged from its wheels while being used in an attempt to identify secondary plant leakage inside the containment bio-wall. The inspectors reviewed the 10 CFR 50.59 screening and technical evaluation to verify that the modification had not affected system operability or availability. The inspectors reviewed associated plant drawings and UFSAR documents impacted by this modification and discussed the changes with licensee personnel to verify that the installation was consistent with the modification documents. The inspectors reviewed photographs of the robot location to determine if conditions resulted in any potential unsafe conditions not described in the engineering change documentation. Additionally, the inspectors verified that problems associated with modifications were being identified and entered into the CAP.

  • EC 281021, Irretrievable Robot in U4 Containment

b. Findings

No findings were identified.

==1R19 Post Maintenance Testing

a. Inspection Scope

==

For the five post maintenance tests and associated work orders (WO) listed below, the inspectors reviewed the test procedures and either witnessed the testing or reviewed test records to determine whether the scope of testing adequately verified that the work performed was correctly completed and demonstrated that the affected equipment was operable. The inspectors verified that the requirements in licensee procedure 0-ADM-737, Post Maintenance Testing, were incorporated into the test requirements. The inspectors reviewed the following WOs consisting of three inspection samples:

  • WO 40296179, 4B component cooling water pump realignment

b. Findings

No findings were identified.

==1R20 Refueling and Other Outage Activities

Unit 3 Refueling Outage PT3-27

a. Inspection Scope

==

Outage Planning, Control and Risk Assessment

During daily outage planning activities by the licensee, the inspectors reviewed the risk reduction methodology employed by the licensee during various refueling outage (RFO)

PT3-27 meetings including outage control center (OCC) morning meetings, operations daily team meetings, and schedule performance update meetings. The inspectors examined the licensee implementation of shutdown safety assessments during PT3-27 in accordance with administrative procedure ADM-51, Outage Risk Assessment and Control, to verify if a defense in depth concept was in place to ensure safe operations and avoid unnecessary risk. In addition, the inspectors regularly monitored outage planning and control activities in the OCC, and interviewed responsible OCC management personnel during the outage to ensure system, structure, and component configurations, and work scope were consistent with TS requirements, site procedures, and outage risk controls.

Shutdown, Cooldown, and Transition to Mode 5 Activities

The inspectors observed selected Unit 3 shutdown, cooldown, and mode transition activities starting on March 17, 2014. The inspectors verified that activities were performed in accordance with the outage plan and associated plant procedures. The inspectors evaluated specific performance attributes including operator performance, communications, and risk management. The inspectors evaluated the following activities:

  • Verified that the plant cooldown was conducted in accordance with licensee procedure 3-OSP-041.7, Reactor Coolant System Heatup and Cooldown Temperature Verification

Monitoring of Shutdown Activities

The inspectors performed walkdowns of important systems and components used for decay heat removal from the spent fuel pool during the shutdown period including the intake cooling water system, component cooling water system, and spent fuel pool cooling system.

Outage Activities

The inspectors examined outage activities to verify that they were conducted in accordance with TS, licensee procedures, and the licensees outage risk control plan.

Some of the more significant inspection activities accomplished by the inspectors were as follows:

  • Walked down selected safety-related equipment clearance orders
  • Verified operability of reactor coolant system pressure, level, flow, and temperature instruments during various modes of operation
  • Verified electrical systems availability and alignment
  • Evaluated implementation of reactivity controls
  • Examined foreign material exclusion (FME) controls put in place inside containment (e.g., around the refueling cavity, near sensitive equipment and RCS breaches) and around the spent fuel pool (SFP)

Refueling Activities and Containment Closure

The inspectors witnessed selected fuel handling operations being performed in accordance with TS and applicable operating procedures from the main control room, refueling cavity inside containment, and the spent fuel pool bridge. The inspectors also examined licensee activities to control and track the position of each fuel assembly. The inspectors evaluated the licensees ability to close the containment equipment, personnel, and emergency hatches in a timely manner per procedure 2-MMP-68.02, Containment Closure.

Corrective Action Program

The inspectors reviewed ARs generated during PT3-27 to evaluate the licensees threshold for initiating ARs. The inspectors reviewed CRs to verify priorities, mode holds, and significance levels were assigned as required. Resolution and implementation of corrective actions of several ARs were also reviewed for completeness. The inspectors routinely reviewed the results of quality assurance (QA)daily surveillances of outage activities.

b. Findings

No findings were identified.

==1R22 Surveillance Testing

a. Inspection Scope

==

The inspectors either reviewed or observed the following five surveillance tests to verify that the tests met the TS requirements, the UFSAR description, the licensees procedural requirements, and demonstrated the systems were capable of performing their intended safety functions and operational readiness. In addition, the inspectors evaluated the effect of the testing activities on the plant to ensure that conditions were adequately addressed by the licensee staff and that after completion of the testing activities, equipment was returned to the status required for the system to perform its safety function. The inspectors verified that surveillance issues were documented in the licensees CAP. The inspectors reviewed the following tests:

Surveillance Test:

  • 3-OSP-023.1, 3A EDG monthly test
  • 4-OSP-059.1, Unit 4 quadrant power tilt ratio (QPTR)
  • 4-OSP-023.1, 4B EDG monthly test

In-Service Tests:

  • 4-OSP-055.1, 4C emergency containment cooler (ECC) quarterly valve in-service test (IST)

RCS Leak Detection Test:

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness (EP)

1EP2 Alert and Notification System Evaluation

a. Inspection Scope

The inspectors evaluated the adequacy of the licensees methods for testing the alert and notification system in accordance with NRC Inspection Procedure 71114, 02, Alert and Notification System (ANS) Testing. The applicable planning standard, 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50, Appendix E, Section IV.D requirements were used as reference criteria. The criteria contained in NUREG-0654, Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and Preparedness in Support of Nuclear Power Plants, Revision 1, were also used as a reference.

The inspectors reviewed various documents which are listed in the Attachment.

Inspectors interviewed personnel involved with siren system maintenance and observed annual siren maintenance field activities. This inspection activity satisfied one inspection sample for the alert and notification system on a biennial basis.

b. Findings

No findings were identified.

1EP3 Emergency Preparedness Organization Staffing and Augmentation System

a. Inspection Scope

The inspectors reviewed the licensees Emergency Response Organization (ERO)augmentation staffing requirements and process for notifying the ERO to ensure the readiness of key staff for responding to an event and timely facility activation. The qualification records of key position ERO personnel were reviewed to ensure all ERO qualifications were current. A sample of problems identified from augmentation drills or system tests performed since the last inspection was reviewed to assess the effectiveness of corrective actions.

The inspection was conducted in accordance with NRC Inspection Procedure 71114, 03, Emergency Preparedness Organization Staffing and Augmentation System. The applicable planning standard, 10 CFR 50.47(b)(2), and its related 10 CFR 50, Appendix E requirements were used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the ERO staffing and augmentation system on a biennial basis.

b. Findings

No findings were identified.

1EP4 Emergency Action Level and Emergency Plan Changes

a. Inspection Scope

Since the last NRC inspection of this program area, no changes have been made to the Radiological Emergency Plan or Emergency Action Levels. The licensee did make several changes to emergency plan implementing procedures and determined that, in accordance with 10 CFR 50.54(q), the changes made in these revisions resulted in no reduction in the effectiveness of the Plan, and that the Plan continued to meet the requirements of 10 CFR 50.47(b) and Appendix E to 10 CFR Part 50. The inspectors conducted a sampling of the implementing procedure changes made between September 1, 2013, and January 15, 2014, to evaluate for potential reductions in the effectiveness of the Plan. However, this review was not documented in a Safety Evaluation Report and does not constitute formal NRC approval of the changes.

Therefore, these changes remain subject to future NRC inspection in their entirety.

The inspection was conducted in accordance with NRC Inspection Procedure 71114, 04, Emergency Action Level and Emergency Plan Changes. The applicable planning standards of 10 CFR 50.47(b), and its related requirements in 10 CFR 50, Appendix E, were used as reference criteria.

The inspectors reviewed various documents that are listed in the Attachment to this report. This inspection activity satisfied one inspection sample for the emergency action level and emergency plan changes on an annual basis.

b. Findings

No findings were identified.

1EP5 Maintenance of Emergency Preparedness

a. Inspection Scope

The inspectors reviewed the corrective actions identified through the Emergency Preparedness program to determine the significance of the issues, the completeness and effectiveness of corrective actions, and to determine if issues were recurring. The licensees post-event action reports, self-assessments, and audits were reviewed to assess the licensees ability to be self-critical, thus avoiding complacency and degradation of their emergency preparedness program. Inspectors reviewed the licensees 10 CFR 50.54(q) change process, personnel training, and selected screenings and evaluations to assess adequacy. The inspectors toured facilities and reviewed equipment and facility maintenance records to assess licensees adequacy in maintaining them. The inspectors evaluated the capabilities of selected radiation monitoring instrumentation to adequately support Emergency Action Level (EAL)declarations.

The inspection was conducted in accordance with NRC Inspection Procedure 71114.05, Maintenance of Emergency Preparedness. The applicable planning standards, related 10 CFR 50, Appendix E requirements, and 10 CFR 50.54(q) and

(t) were used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment. This inspection activity satisfied one inspection sample for the maintenance of emergency preparedness on a biennial basis.

1EP6 Drill Evaluation

Emergency Preparedness Drill

a. Inspection Scope

On February 6, 2014, the inspectors observed an emergency preparedness drill and the performance of the licensees emergency response organization. The drill included a simulated damaged irradiated fuel assembly in the spent fuel pit of Unit 3, a failed steam pressure transmitter resulting in a transient that resulting in a fuel barrier failure. The fuel barrier failure required a site area emergency declaration and notification to state and local county officials, and the NRC per licensee procedure 0-EPIP-20101, Duties of the Emergency Coordinator. The scenario progressed to the loss of the reactor coolant pressure boundary barrier after a large break loss of coolant accident occurred requiring a general emergency declaration and an additional notification. The inspectors observed the crew in the plant simulator including simulated implementation of emergency procedures. The inspectors observed the emergency response organization staff in the technical support center (TSC) and emergency operations facility (EOF) while they implemented the event classification guidelines and emergency response procedures. The inspectors determined that the emergency classification and notifications were made in accordance with the licensee emergency plan implementing procedure 0-EPIP-20101. The inspectors attended the licensees post drill critique, reviewed the licensees critique items, and discussed inspector observations with the licensee to verify that drill issues were identified and captured in the licensees corrective action program.

b. Findings

No findings were identified.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (IP 71151)

.1 Initiating Events Cornerstone

a. Inspection Scope

The inspectors reviewed licensee submittals for the Unit 3 and Unit 4 performance indicators (PI) listed below for the period January 1, 2013, through December 31, 2013, to verify the accuracy of the PI data reported during that period. Performance indicator definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, and licensee procedure 0-ADM-032, NRC Performance Indicators Turkey Point, were used to check the reporting for each data element. The inspectors checked operator logs, plant status reports, condition reports, system health reports, and PI data sheets to verify that the licensee had identified the required data, as applicable.

The inspectors interviewed licensee personnel associated with performance indicator data collection, evaluation, and distribution.

  • Unit 3 Unplanned Scrams per 7000 Critical Hours
  • Unit 4 Unplanned Scrams per 7000 Critical Hours
  • Unit 3 Unplanned Scrams with Complications
  • Unit 4 Unplanned Scrams with Complications

b. Findings

No findings were identified.

.2 Emergency Preparedness Cornerstone

a. Inspection Scope

The inspectors sampled licensee submittals relative to the PIs listed below for the period April 1, 2013, through September 30, 2013. To verify the accuracy of the PI data reported during that period, PI definitions and guidance contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 6, were used to confirm the reporting basis for each data element.

  • Emergency Response Organization (ERO) Drill/Exercise Performance
  • ERO Drill Participation
  • Alert and Notification System Reliability

For the specified review period, the inspectors examined data reported to the NRC, procedural guidance for reporting PI information, and records used by the licensee to identify potential PI occurrences. The inspectors verified the accuracy of the PI for ERO drill and exercise performance through review of a sample of drill and event records.

The inspectors reviewed selected training records to verify the accuracy of the PI for ERO drill participation for personnel assigned to key positions in the ERO. The inspectors verified the accuracy of the PI for alert and notification system reliability through review of a sample of the licensees records of periodic system tests. The inspectors also interviewed the licensee personnel who were responsible for collecting and evaluating the PI data. Licensee procedures, records, and other documents reviewed within this inspection area are listed in the Attachment. This inspection satisfied three inspection samples for PI verification on an annual basis.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution (IP 71152)

.1 Daily Review

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems, and to help identify repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed a screening of items entered daily into the licensees corrective action program. This review was accomplished by reviewing daily printed summaries of ARs and by reviewing the licensees electronic AR database.

Additionally, RCS unidentified leakage was checked on a daily basis to verify no substantive or unexplained changes. Documents reviewed are listed in the Attachment.

b. Findings

No findings were identified.

.2 Annual Sample:

Root Cause Evaluation Associated With Component Cooling Water to Residual Heat Removal Weld Leak on Piping for RV-4-747B

a. Inspection Scope

The inspectors selected the root cause evaluation for AR 01931761, CCW Pipe Leak Upstream of RV-4-747B, 4B RHR Heat Exchanger Return Relief Valve, for a more in-depth review of the circumstances and the corrective actions that followed. The root cause report was reviewed to ensure that an appropriate evaluation was performed and corrective actions were specified and prioritized in accordance with the licensees program. Other attributes checked included disposition of operability and resolution of the problem including cause determination and corrective actions. The inspectors evaluated the condition report in accordance with the requirements of the licensees corrective actions process as specified in licensees procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action.

b. Findings and Observations

Introduction:

A Green self-revealing non-cited violation (NCV) of 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, was identified when the licensee failed to implement corrective actions that addressed the low stress high cycle fatigue of component cooling water (CCW) relief valve RV-4-747B piping caused by flow induced vibration. As a result, CCW system flow induced vibration resulted in weld cracks and system pressure boundary leakage in January 2014.

Description:

On November 18, 2012, plant personnel identified a weld leak of 5 to 10 drops per minute at the relief valve RV-4-747B piping branch connection on the 16 inch CCW piping. This leak was at the same location where the weld had been previously repaired in November 2011. The licensee entered the leak into the CAP as AR 1824939 and performed an apparent cause evaluation which concluded that there was significant movement of the Unit 4 CCW relief valve RV-4-747B piping while residual heat removal (RHR) was in service. Failure of the weld was due to low stress high cycle fatigue caused by flow induced vibration. In February 2013, the licensee repaired the branch connection weld leak while Unit 4 was in a refueling outage. A corrective action was assigned to engineering to evaluate the need for pipe supports to reduce the effects from the flow induced vibration on the piping. A pipe support was installed in June 2013 at RV-4-747B under engineering change (EC) 278231; however, the analysis used to design the support did not validate the effectiveness of the support to reduce vibration effects to an acceptable level. On January 8, 2014, plant operations identified a 0.0024 gallon per minute leak on the toe of the weld on the half coupling connection between the 1 inch piping upstream of RV-4-747B and 16 inch CCW discharge pipe of the 4B RHR heat exchanger. This leak location was in the same location as the previous leaks identified in 2011 and 2012. The licensee entered the leak into the CAP as AR 1931761 and performed a root cause evaluation which concluded the failure mechanism of the cracked weld was the same as the previous weld failure in 2012 and 2011 which was low stress high cycle fatigue. The cause of the fatigue was determined to be elevated system pressure transients during pump in-service tests combined with potentially degraded relief valve operation which resulted in excessive vibration in the 1 inch relief valve inlet line.

Analysis:

The failure to implement corrective actions that reduced low stress high cycle fatigue of CCW relief valve RV-4-747B piping caused by flow induced vibration was a performance deficiency. The performance deficiency was more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to implement adequate corrective actions to address CCW system flow induced vibration resulted in weld cracks and CCW system pressure boundary leakage in January 2014. The finding was screened using Exhibit 1, Mitigating Systems Screening Questions, found in Inspection Manual Chapter 0609, Significance Determination Process, Appendix A, Significance Determination Process for Findings At-Power (June 19, 2012). The inspectors determined the finding was of very low safety significance (Green) because the finding did not affect design or qualification, did not represent a loss of system function, and did not represent an actual loss of function of a technical specification train of equipment. The finding was associated with a cross-cutting aspect in the evaluation component of the problem identification and resolution area because the licensee did not thoroughly evaluate issues and corrective actions from previous weld failures on CCW system RV-4-747B piping caused by flow induced vibration (P.2).

Enforcement:

10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires in part that measures shall be established to assure conditions adverse to quality are promptly identified and corrected. Contrary to the above, in November 2011 and November 2012, the licensee identified that the 4B CCW relief valve piping to the 4B RHR heat exchanger experienced system pressure boundary leakage due to low stress high cycle fatigue caused by flow induced vibration on the line, but failed to implement corrective actions that addressed the flow induced vibration. The failure to correct the flow induced vibration resulted in a weld failure in the CCW relief valve piping in January 2014. The licensee repaired the weld failures, implemented special instructions to minimize the time that split header operation was performed, and developed a plan to replace the existing relief valve with an orifice or alternate relief valve. This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy, because it was of very low safety significance and was entered in the licensees corrective action program as AR 1931761 to address recurrence. (NCV 05000251/2014002-01 Failure to Take Adequate Corrective Actions to Correct Flow Induced Vibration Leads to CCW Piping Weld Failure).

.3 Annual Sample:

Root Cause Evaluation Associated with PT-3-495 Out of Calibration

a. Inspection Scope

The inspectors selected root cause evaluation for AR 01930745, PT-3-495 found out of calibration during 3-SMI-072.02, for a more in-depth review of the circumstances and the corrective actions that followed. The root cause report was reviewed to ensure that an appropriate evaluation was performed and corrective actions were specified and prioritized in accordance with the licensees program. Other attributes checked included disposition of operability and resolution of the problem including cause determination and corrective actions. The inspectors evaluated the condition report in accordance with the requirements of the licensees corrective actions process as specified in licensees procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205, Condition Evaluation and Corrective Action.

b. Findings and Observations

Introduction:

A Green self-revealing non-cited violation (NCV) of TS Section 3.3.2, Engineered Safety Features Actuation Instrumentation, (ESF) was identified when the licensee failed to perform the channel calibration of Unit 3 ESF steam pressure protection channel III within the required 18-month frequency. When the surveillance was performed, the licensee determined that steam generator pressure transmitter PT-3-495 needed to be replaced due to excessive drift. The licensee considered PT-3-495 to have been inoperable for approximately 10 months going back to the original due date of the channel calibration.

Description:

On December 13, 2013, during the performance of a functionality review for an unrelated issue, it became readily apparent to the licensee that channel calibration procedure 3-SMI-072.2, P-3-466, P-3-475, P-3-485, and P-3-495 Steam Pressure Channel Calibration, Protection Channels, had not been performed for approximately 31 months. Technical Specification 3.3.2 and Table 4.3-2 required that a channel calibration be performed on channels with input to ESF every 18 months. On April 15, 2013, during the Unit 3 extended power uprate (EPU) outage, the licensee credited completion of the Unit 3 main steam line pressure transmitter channel calibration for P-3-495 in the surveillance tracking program (STP) in error. The licensee normally tracked completion of TS surveillance requirements by completion of dedicated work orders, but in this case a partial performance of the channel calibration was imbedded in a larger work order. On discovery of the missed channel calibration, the licensee applied the provision of TS 4.0.3 for a missed TS surveillance test of P-3-495. Accordingly, the licensee performed a risk evaluation which determined that completion of the surveillance could be delayed up to the specified 18-month surveillance interval for the test without a significant increase in risk to the plant. In October 2013, the licensee performed loss of fill oil preventive maintenance (PM) check 003PM095033, U3 Rosemount Transmitter Surveillance Program, for P-3-495 and identified that the transmitter needed to be calibrated or replaced as soon as possible based on increasing drift. The licensee generated an AR to track replacement of the transmitter, but the AR was canceled and scheduled by maintenance to be replaced the next time the instrument was removed from service. The inspectors observed that the licensees missed surveillance risk evaluation for P-3-495 did not consider the degradation identified during this October PM task. On January 3, 2014, while performing 3-SMI-072.2 for Unit 3 steam break protection channel III, main steam line pressure transmitter PT-3-495 was found outside of the procedural acceptance criteria due to pressure transmitter drift. Transmitter PT-3-495 provides the C steam generator channel III pressure signal used for the ESF steam line isolation signal to mitigate a steam break design basis accident. Transmitter PT-3-495 was replaced, calibrated successfully, and returned to service on January 4, 2014. The licensee determined that the transmitter and associated instrument channel were inoperable from March 9, 2013 (the time of the due date for the missed surveillance), until the date of repair. The licensee concluded that the overall ESF steam pressure protection signal was operable since both redundant steam pressure protection channels II and IV remained available and were demonstrated to be operable by the successful performance of their respective surveillances. During the period of inoperability, the instrument channel associated with PT-3-495, Channel III remained in service and exceeded the allowed outage time of 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> to place the channel in the tripped condition and the shutdown actions of TS 3.0.3 were not entered. As a result, the licensee submitted LER 05000250/2014-001-00 in accordance with 10CFR50.73(a)(2)(i)(B) as a condition prohibited by TS. The inspectors determined that the issue was self-revealing because the condition became readily apparent to the licensee during the performance of a functionality review for an unrelated issue. Additionally, the inspectors concluded that the licensee had missed an opportunity to address degradation of the instrument following the completion of the October 2013 PM.

The licensees root cause evaluation (RCE) determined the cause of this event to be the deviation from the normal process of using a dedicated work order (WO) to satisfy surveillance requirements. This created a situation where there was no second verifier to ensure that surveillance test requirements had been satisfactorily completed. This issue was placed in the licensees CAP as AR 1938191. Corrective actions completed (or planned) included:

(1) replacing PT-3-495,
(2) performing an extent of condition on all other work orders completed during the extended power uprate (EPU) outage to ensure TS compliance and
(3) revising the surveillance tracking program procedure to verify that a surveillance test has been completed when crediting non-dedicated work orders.
Analysis:

The failure to perform the channel calibrations associated with 3-SMI-072.2 within the 18-month TS requirement was a performance deficiency. The performance deficiency was more than minor because it was associated with the human performance attribute of the mitigating systems cornerstone and affected the cornerstone objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the failure to perform the channel calibration surveillance test procedure for transmitter PT-3-495 within the 18-month required frequency resulted in 10 months of channel inoperability. The finding was screened using Exhibit 1, Mitigating Systems Screening Questions, found in Inspection Manual Chapter 0609, Significance Determination Process, Appendix A, Significance Determination Process for Findings At-Power (June 19, 2012). The inspectors determined the finding was of very low safety significance (Green) because the finding did not affect design or qualification, did not represent a loss of system function, and did not represent an actual loss of function of a TS train of equipment. The finding was associated with a cross-cutting aspect in the work management component of the human performance area because the licensee failed to implement their process for planning, controlling, and executing required surveillance tests (H.5).

Enforcement:

Turkey Point Nuclear Plant Unit 3 TS surveillance requirement 3.3.2, Engineered Safety Features Actuation Instrumentation, Table 4.3-2 requires in part that instrument operability be demonstrated by successful completion of a channel calibration of the ESF steam line pressure protection channel every 18 months. If the instrument channel is determined to be inoperable, TS 3.3.2 allows continued operation until the next required performance of the analog channel operational test provided that the inoperable channel is placed in trip within six hours. Contrary to the above, from April 25, 2011, to January 3, 2014, Turkey Point failed to perform the required channel calibration of Unit 3 steam line protection channel III, and failed to perform the required actions of TS LCO 3.3.2 when operability was no longer supported on March 9, 2013.

This violation is being treated as an NCV, consistent with Section 2.3.2 of the Enforcement Policy. The violation was entered into the licensees CAP as AR 1938191 (NCV 05000250/2014002-02 TS Channel Calibration of ESF Steam Line Protection Channel III Not Performed).

4OA3 Follow-up of Events and Notice of Enforcement Discretion (IP 71153)

.1 (Closed) Licensee Event Report (LER) 05000250/2013-009-00, Loose Breaker Control

Power Fuse Holder Caused 3B ICW Pump to be Inoperable Longer than Allowed Outage Time

a. Inspection Scope

The LER documented that the 3B Intake Cooling Water (ICW) pump was inoperable for a period of time that was greater than allowed by TS. The licensee determined that the total OOS time for the 3B ICW pump was 4 days which exceeded the TS allowed outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The inspectors reviewed the LER and the associated corrective action document (AR 1929130) to verify the accuracy and completeness of the LER and the appropriateness of the licensees corrective actions. The inspectors also reviewed the LER and AR to identify any licensee performance deficiencies associated with the issue.

b. Findings

On September 28, 2013, while Unit 3 was in Mode 1, operators discovered that power to the 3B intake cooling water (ICW) pump breaker closing circuit and charging springs was lost. The under current (UC) fuse holder was noted to be slightly backed out and not firmly in place which resulted in the loss of breaker control power. Control power was restored after the fuse holder was pressed back in place on September 29, 2013.

The licensee performed an investigation that determined that the 3B ICW pump had been inoperable for approximately four days (the time the pump was last started until the fuse holder was fully re-inserted), which was longer than the allowed TS 3.7.3, Intake Cooling Water System, outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. Although operators performed a daily verification that the breaker control power available white indicating light was lit on the breaker cubicle, the licensee determined that reasonable assurance could not be established that the fuses had enough contact with the base to ensure power to the closing spring even though the white control power light was lit. Therefore, the licensee concluded that the 3B ICW pump was inoperable for four days prior to discovery of the fuse holder condition. The inspectors determined the ICW system would have been able to perform its function even with the 3B ICW pump inoperable. The 3A and 3C ICW pumps were available and only one ICW pump is needed to remove design basis heat loads. Based on the availability of the ICW system to perform its heat removal function; and the relatively short duration of the condition prior to its discovery on September 28, the inspectors concluded that the event was of very low safety significance.

The inspectors determined that a violation of TS limiting condition for operation (LCO)3.7.3, Intake Cooling Water System, occurred since Unit 3 was in Mode 1 and the 3B ICW pump was not returned to an operable status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or the unit shut down and placed in hot standby within the next six hours. Although a violation of the TS LCO occurred, the violation was not attributable to an equipment failure that was avoidable by reasonable licensee quality assurance measures or management controls. The inspectors concluded that the violation would normally be characterized as Severity Level IV based on its very low safety significance. The NRC exercised enforcement discretion (Enforcement Action (EA)-14-058) in accordance with Section 2.2.4.d of the Enforcement Policy because the violation was not associated with a licensee performance deficiency; and therefore, it will not be considered in the assessment process or the NRCs Action Matrix. This issue is documented in the licensees CAP as AR 1929130. Corrective actions included an investigation of the material condition of the fuse holder and base assembly, and a revision to the breaker operation procedure to include additional guidance on validating proper installation of the fuse holder when racking in a four kilovolt breaker. The LER is closed.

.2 (Closed) LER 05000250/2013-008-00, Through-Wall Leak in 3A CCW Pump Threaded

Fitting Caused Pump to be Inoperable Longer than Allowed Outage Time

a. Inspection Scope

The LER documented that the 3A component cooling water (CCW) pump was inoperable for a period of time that was greater than allowed by TS. The licensee determined that the total out of service time for the 3A CCW pump was 12 days which exceeded the TS allowed outage time of 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The inspectors reviewed the LER and the associated corrective action documents (AR 1880602 and 1880576) to verify the accuracy and completeness of the LER and the appropriateness of the licensees corrective actions. The inspectors also reviewed the LER and ARs to identify any licensee performance deficiencies associated with the issue.

b. Findings

On June 7, 2013, Unit 3 was at 100 percent reactor power when the licensee identified a small leak of approximately 100 drops per minute at a threaded pipe connection on the 3A component cooling water pump casing. The licensee considered the pump to be operable because the leakage was within the make-up capacity of the CCW filling system. On June 19, the small leak had worsened to a steady stream of water and the pump was declared inoperable and taken out of service for repair. Upon removal and examination of the pipe, the licensee determined the pipe had a through-wall crack requiring replacement. The licensees root cause analysis for the piping failure was documented in action request 1880602 and was previously reviewed by the inspectors.

The inspectors determined that the licensee had failed to identify and correct a flaw that resulted in through-wall pressure boundary leakage. The enforcement aspects of that issue were documented in NRC inspection report 2013003 (ADAMS accession number ML13211A151).

Based on information gained from forensic examination of the failed pipe, the licensee determined that the pump would have been inoperable from the time the leak first became apparent on June 7, 2013. Although the pipe flaw size did not exceed acceptance criteria and the 3A CCW pump remained capable of performing its function, the licensee could not establish a reasonable degree of assurance that the flaw would not have increased in size during the mission time of the pump. TS limiting condition of operation (LCO) 3.7.2, Component Cooling Water, requires three CCW pumps be operable in Modes 1 through 4, and with one inoperable pump, the two remaining pumps must be powered from independent power supplies within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or the unit shut down and placed in hot standby within six hours. Contrary to this requirement, the operable 3B and 3C CCW pumps were powered from the 3B safety related electrical bus for approximately 12 days with the 3A CCW pump in an inoperable condition. The inspectors utilized available risk-informed tools to assess the safety significance of the 3A CCW pump inoperability. Based on the availability of the 3B and 3C CCW pumps and the relatively short amount of time that the 3A CCW pump would have been considered inoperable, the inspectors concluded this event was of very low safety significance.

The inspectors determined in this case that there was no performance deficiency associated with the TS violation because the licensee monitored the leak for degradation and took action to declare the pump inoperable when it worsened. Additionally, the information obtained from forensic examination of the pipe flaw to assess the historical operability of the pump was not available to the licensee until after the condition had been repaired. The inspectors concluded that the violation would normally be characterized as Severity Level IV based on its very low safety significance. Although a violation of TS occurred, the violation was not attributable to an equipment failure that was avoidable by reasonable licensee quality assurance measures or management controls. The NRC exercised enforcement discretion (EA-14-058) in accordance with Section 2.2.4.d of the Enforcement Policy because the violation was not associated with a licensee performance deficiency. Therefore, it will not be considered in the assessment process or the NRCs Action Matrix. This violation was documented in the licensees CAP as AR 1883690. Licensee corrective actions included:

(1) replacement of the leaking pipe on 3A CCW pump,
(2) evaluations to replace similar CCW pump casing schedule 40 pipe nipples with schedule 80 and,
(3) formal evaluations of existing leaks at threaded connections on Class 1, 2, and 3 systems to consider the potential for through-wall flaws. The LER is closed.

.3 (Closed) LER 05000250/2014-001-00, Missed Surveillance Test Resulted in a Steam

Generator Pressure Instrument Channel to be Inoperable Longer than Allowed Outage Time

On January 3, 2014, Unit 3 was in Mode 1 at 100 percent reactor power when the instrument channel associated with Main Steam Line Pressure Transmitter PT-3-495 was found outside procedural acceptance criteria due to pressure transmitter (PT) drift.

The surveillance for this instrument was considered a missed surveillance at the time of performance since it had not been completed for approximately 32 months and it had an 18-month TS requirement. The channel associated with PT-3-495 was considered inoperable from the time of replacement, January 3, 2014, back to the due date of the missed surveillance, March 9, 2013. PT-3-495 was replaced, calibrated successfully, and returned to service on January 4, 2014. The licensee determined the root cause of the event to be the deviation from the normal process of using a dedicated work order (WO) to satisfy surveillance requirements. Corrective actions included replacing PT-3-495, performing an extent of condition on all other work orders completed during the extended power uprate (EPU) outage to ensure TS compliance, and revising the surveillance tracking program procedure to verify that a surveillance test has been completed when crediting non-dedicated work orders. This event was associated with a violation of very low safety significance. The enforcement aspects associated with this LER are discussed in Section 4OA2 of this report. The LER is closed.

4OA5 Other Activities

.1 (Closed) Temporary Instruction 2515/182 - Review of the Industry Initiative to Control

Degradation of Underground Piping and Tanks

a. Inspection Scope

The inspectors conducted a review of records and procedures related to the licensees program for buried piping and underground piping and tanks in accordance with Phase II of Temporary Instruction (TI) 2515-182 to confirm that the licensees program contained attributes consistent with Sections 3.3.A and 3.3.B of Nuclear Energy Institute (NEI) 09-14, Guideline for the Management of Buried Piping Integrity, Revision 3, and to confirm that these attributes were scheduled to be completed by the NEI 09-14, Revision 3, deadlines. The inspectors interviewed licensee staff responsible for the buried piping program and reviewed activities related to the buried piping program to determine if the program was managed in a manner consistent with the industrys buried piping initiative.

The licensees buried piping and underground piping and tanks program was inspected in accordance with paragraph 03.02.a of the TI and it was confirmed that activities which correspond to completion dates specified in the program which have passed since the Phase I inspection was conducted, have been completed. The licensees buried piping and underground piping and tanks program was inspected in accordance with paragraph 03.02.b of the TI and responses to specific questions found in http://www.nrc.gov/reactors/operating/ops-experience/buried-pipe-ti-phase-2-insp-req-2011-11-16.pdf were submitted to the NRC headquarters staff.

b. Findings

No findings were identified. Based upon the scope of the review described above, Phase II of TI-2515/182 was completed.

.2 Cross-Cutting Aspect Cross-Reference

The table below provides a cross-reference from the 2013 third and fourth quarter findings and associated cross-cutting aspects to the new cross-cutting aspects resulting from the common language initiative. These aspects and any others identified since January 2014 will be evaluated for cross-cutting themes and potential substantive cross-cutting issues in accordance with Inspection Manual Chapter (IMC) 0305 starting with the 2014 mid-cycle assessment review.

Finding Old Cross-Cutting Aspect

New Cross-Cutting Aspect 05000250/2013004-01 H.2(c)

H.7 05000250/2013004-02 H.4(c)

H.2 05000250/2013004-03 H.3(a)

H.5 05000251/2013004-04 H.4(b)

H.8 05000250/2013004-05 H.2(c)

H.7 05000251/2013005-01 H.3(a)

H.5

4OA6 Meetings

The resident inspectors presented the inspection results to Mr. Kiley and other members of licensee management on April 10, 2014. The inspectors asked the licensee whether any of the material examined during the inspection should be considered proprietary information. The licensee did not identify any proprietary information.

ATTACHMENT: SUPPPLEMENTAL INFORMATION KEY POINTS OF CONTACT

Licensee Personnel:

F. Banks, Quality Manager H. Benitez, PTN Engineering - Underground Piping Program Manager G. Bowen, EP staff C. Cashwell, Radiation Protection Manager T. Conboy, Plant General Manager P. Czaya, Licensing D. Dell, EP Staff C. Domingos, Engineering Director M. Downs, EP staff T. Eck, Security Manager K. Ellmers, Sr. Siren Technician M. Epstein, Emergency Preparedness Manager D. Funk, Operations Manager O. Hanek, Licensing Engineer M. Jones, System Engineering Manager M. Katz, Maintenance Manager M. Kiley, Site Vice-President S. Mihalakea, Licensing D. Mothena, Emergency Preparedness Corporate Functional Area Manager N. Rios, Chemistry Manager D. Sluzka, Work Controls Manager B. Stamp, Training Manager R. Tomonto, Licensing Manager M. Wayland, Operations Director J. Wingate, EP staff

NRC Personnel:

C. Evans, Region II Legal Counsel and Enforcement Officer J. Hanna, Senior Risk Analyst, Division of Reactor Safety S. Sandal, Senior Project Engineer T. Su, Reactor Engineer

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened and Closed 05000250/2014002-01

05000250/2014002-02 NCV

NCV Failure to Take Adequate Corrective Actions to Correct Flow Induced Vibration Leads to CCW Piping Weld Failures.

(Section 4OA2.2)

TS Channel Calibration of ESF Steam Line Protection Channel III Not Performed (Section 4OA2.3)

Closed

05000250/2013-009-00

05000250/2013-008-00

05000250/2014-001-00

05000250, 251/2515/182 LER

LER

LER

TI Loose Breaker Control Power Fuse Holder Caused 3B ICW Pump to be Inoperable Longer than Allowed Outage Time (Section 4OA3.1)

Through-Wall Leak in 3A CCW Pump Threaded Fitting Caused Pump to be Inoperable Longer than Allowed Outage Time (Section 4OA3.2)

Missed Surveillance Test Resulted in a Steam Generator Pressure Instrument Channel to be Inoperable Longer than Allowed Outage Time (Section 4OA3.3)

Review of the Industry Initiative to Control Degradation of Underground Piping and Tanks (Section 4OA5.1)

LIST OF

DOCUMENTS REVIEWED

Action Requests:

01939933

01946565

01939548

01944754

01946589

01933839

01940963

01942544

01938704

01941033

01942618

01945528

01944767

01946385

01938123

01947210

01945663

01937543

01947219

01945746

01937722

01947489

01947747

01935879

01946040

01947063

01935975

01946270

01947139

01936028

01946324

01946076

01933286

01946524

01946078

01933231

01946660

01946217

01932528

01945718

01946225

01942421

01945773

01946303

01945968

01942398

Section 1R04: Equipment Alignment

P&ID 5610-M-3075, Auxiliary Feedwater (AFW) System Turbine Drive for AFW Pumps

Turkey Point System Description 117, Auxiliary Feedwater System

P&ID 5613-M-3022, Emergency Diesel Engine and Oil System

3-OP-023, Emergency Diesel Generator

3-NOP-022, Emergency Diesel Generator Fuel Oil System

4-OSP-075.5, Auxiliary Feedwater System Flow Path Verification

3-OSP-075.5, Auxiliary Feedwater System Flow Path Verification

P&ID 5613-M-3062, Safety Injection System

Section 1R05: Fire Protection

0-ONOP-016.10, Pre-Fire Plan Guidelines and Safe Shutdown Manual Actions

Section 1R06: Flood Protection Measures

Drawing 5610-C-1695, Network of Barriers for External Flood Protection

0-SMM-102.1, Flood Protection Stop Log and Penetration Seal Inspection

Section 1R15: Operability Evaluations

EN-AA-203-1001, Operability Determinations and Assessments

0-ADM-226, Operability Screening and Condition Reports

0-ADM-213, Technical Specification Related Equipment Out of Service Logbook

Section 1R18: Plant Modifications

0-ADM-009, Containment Closeout Inspection

Section 1R19: Post Maintenance Testing

0-ADM-737, Post Maintenance Testing

4-SMI-059.08A, Power Range Nuclear Instrumentation Protection Channel N-4-41 Calibration

0-CMP-102.01, Troubleshooting and Repair Guidelines

0-CMI-059.10, Excore Neutron Detector Post Installation Inspection and Testing

Section 1R20: Refueling and Other Outage Activities

3-GOP-103, Power Operation to Hot Standby

3-GOP-305, Hot Standby to Cold Shutdown

3-OSP-041.7, Reactor Coolant System Heatup and Cooldown Temperature Verification

0-NOP-038.10, Manipulator Crane Operating Instruction

3-NOP-38.23, Fuel Transfer System Operations

3-NOP-040.02, Refueling Core Shuffle

0-ADM-035, Limitations and Precautions for Handling Fuel Assemblies

MA-AA-101-1000, Foreign Material Exclusion Procedure

3-OP-038.1, Preparation of Refueling Activities

Section 1EP2: Alert and Notification System Evaluation

Procedures and Reports

Turkey Point Radiological Emergency Plan, Rev. 60

EP-SR-102-1000, Nuclear Division Florida Alert and Notification System Guideline, Rev. 8

Siren Maintenance Procedure No. 6.80.02, Rev. I

WPS-4000 Series High Power Voice and Siren System Operating and Troubleshooting Manual

PI-AA-204, Condition Identification and Screening Process, Rev. 22

PI-AA-205, Condition Evaluation and Corrective Actions, Rev. 23

Records and Data

Documentation of Quarterly siren maintenance for 2012 and 2013

Documentation of bi-weekly siren tests and maintenance for 2012 and 2013

Corrective Action Documents

1903495; Siren S-5 Lightning damage

1899615; Siren S-12 Lightning damage

1889287; Siren S-38 loss of communications

1886797; Siren S-28 pole damage

1935265; 2012 annual maintenance data hard drive failure

1935171; Admin errors on ANS documentation

Section 1EP3: Emergency Preparedness Organization Staffing and Augmentation

System

Procedures

EPLAN, Turkey Point Plant Radiological Emergency Plan, Rev. 60

EP-AA-100-1000-1007, Conducting EP Regulatory Reviews, Rev. 1

0-EPIP-20101, 10CFR50.54(q) Screen and Evaluation (ARs: 1892310, Rev. 1, 1901378, and

1892294)

EP-AD-006, Maintaining the Emergency Response Directory (ERD) & Requirements for Manual

Callout Surveillance, Rev. 14

EP-AD-011, Instructions for Maintaining the Emergency Preparedness NRC Performance

Indicators

EP-AD-012, Autodialer Maintenance and Testing Instructions, Rev. 7

EP-AD-015, Emergency Preparedness ERO Staffing Advisory Committee and Training

Committee, Rev. 14

EP-AA-01, Emergency Preparedness Expectations, Rev. 0

Records and Data

2013 and 2014 ERO Team Staff Assignments

2013 off-hour augmentation test reports

Auto-dialer records: 1/8/2014 - 1/22/2014

Corrective Action Documents

1746619; EOF ST/CO Comm. potential to drop below 3

1746623; EOF Fuels Eng. potential to drop below 3

1746630; OSC Dose Recorder potential to drop below 3

1746635; OSC Doc. Control potential to drop below 3

1746638; Duty Call Supervisor potential to drop below 3

1746644; EOF RP Manager potential to drop below 3

1801659; EOF Recovery Manager potential to drop below 3

1898914; EOF RP Manager dropped below 3

Section 1EP4: Emergency Action Level and Emergency Plan Changes

Procedures

Emergency Plan, Rev. 60

0-EPIP-20101, 10CFR50.54(q) Screen and Evaluation, Rev. 1

Change Packages

0-HPS-090, Inventory of Radiation Protection Emergency Equipment, Rev. 2

0-EPIP-20132, Technical Support Center (TSC) Activation and Operation, Rev. 7

Corrective Action Documents

1935172; RCS sampling procedure has no high rad precautions/limitation statements

1908087; Editorial Change to Emergency Coordinator Duties

1908448; Excessive RCS Activity word deletion

27976; Actions if Plant Site Inaccessible

Section 1EP5: Maintenance of Emergency Preparedness

Procedures

EP-AA-100-1001, Guidelines for Maintaining Emergency Preparedness, Rev. 5

0-EPIP-20126, Off-Site Dose Calculations - Extended Power Uprate, Rev.7

0-NCZP-041.1, Obtaining a Reactor Coolant Sample, Rev. 1

EP-AA-105-1000, Equipment Important to Emergency Response, Rev. 0

0-EPIP-20101, Duties of the Emergency Coordinator, Rev. 14

Records and Data

Turkey Point 2014 Emergency Planning public brochure

PTN-12-010, Turkey Point Nuclear Oversight Report

PTN-13-009, Turkey Point Nuclear Oversight Report

AT-01.16, Single AR Report for DEP Opportunity Evaluation for NOUE Declared on 4/2/12

AT-01.16, Single AR Report for Unit 4 Reactor Trip

AT-01.16, Single AR Report for Critique of Notifications during Unusual Event on 4/19/13

2012 10/25 Drill report

2013 August Drill Report

2013 December Drill Report

2013 Ingestion Pathway Evaluation Exercise Report

2013 May Practice Evaluation Exercise Report

Corrective Action Documents

1750814; DEP opportunity had different results than lesson package

1751998; DEP opportunity evaluation for NOUE declared at PTN on 4/2/12

1761448; TSC backup power did not function during loss of normal power

1772978; Concrete ramps located where flood stop logs get installed

1817868; General rollup during EP drill

1867707; Unit 4 Unusual Event - 4/19/13

1869299; Critique of notifications during Unusual Event on 4/19/13

1876973; EP indicator dropped below green

1883638; Dual roles for ERO responders

1884141; EP NRC inspection observations

1891427; EP DEP indicator showing a declining trend in EOF/TSC

1934762; Review E-Plan 5.1.2 regarding post-accident sampling

Section 4OA1: Performance Indicator Verification

Procedures

0-ADM-032, NRC Performance Indicators Turkey Point, Rev. 5

Records and Data

Documentation of DEP opportunities for 2nd -3rd quarter 2013

Documentation of ANS tests for 2nd quarter - 3th quarter 2013

Documentation of drill and exercise participation for 2nd quarter - 3rd quarter 2013

Various ERO Personnel Qualification and Participation records

Corrective Action Documents

1682047, EP self-assessment - NRC drill participation performance indicator improvement

570387, Drill and exercise participation affecting NRC PI

2365, Seven SROs had not participated in a qualified opportunity in 8 quarters

Section 4OA5: Other Activities

Procedures

ER-AA-102, Underground Piping and Tanks Integrity Program, Rev. 6

ER-AA-102-1000, Underground Piping and Tanks Integrity Examination Procedure, Rev. 2

Corrective Action Program Documents

AR 1678662, Generated to Track Actions Associated with Meeting Milestones of NEI 09-14,

Rev. 3

AR 01802204, QHSA for NRC Buried Piping Inspection (TI 2515/182)

AR 1915405, QHSA for NRC Buried Piping Inspection (TI 2515/182 Phase 2)

AR 1915405-01, PTN Response to Enclosure 2 TI-182 Phase 2 Questions

Other Documents

Buried Piping Program Health Report (7/1/2013 - 9/30/2013)

Drawing 5610-C13, Utility Piping - Main Plant Area, Rev. 27

PTN Buried Piping Program Basis Document, Revision 1

Turkey Point Nuclear Station Underground Piping and Tanks Condition Assessment

Plan, Rev. 2

Unit 3 Circulating Water Pipe NDE Inspection, Turkey Point Nuclear Station, by Pure

Technologies, US, August 2012

LIST OF ACRONYMS

AR

Action Request

CAP

Corrective Action Program

CCW

Component Cooling Water

CFR

Code of Federal Regulations

EAL

Emergency Action Level

EDG

Emergency Diesel Generator

IST

Inservice Testing

NAP

Nuclear Administrative Procedure

NRC

Nuclear Regulatory Commission

PI

Performance Indicator

P&ID

Piping and Instrumentation Drawing

RCE

Root Cause Evaluation

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

TS

Technical Specifications

U3

Unit 3

U4

Unit 4

UFSAR

Updated Final Safety Analysis Report

WO

Work Order

GOP

General Operating Procedure

ONOP

Off Normal Operating Procedure