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| number = ML16119A441
| number = ML16119A441
| issue date = 04/28/2016
| issue date = 04/28/2016
| title = Cooper Nuclear Station - NRC Integrated Inspection Report 05000298/2016001
| title = NRC Integrated Inspection Report 05000298/2016001
| author name = Warnick G G
| author name = Warnick G
| author affiliation = NRC/RGN-IV/DRP/RPB-C
| author affiliation = NRC/RGN-IV/DRP/RPB-C
| addressee name = Limpias O A
| addressee name = Limpias O
| addressee affiliation = Nebraska Public Power District (NPPD)
| addressee affiliation = Nebraska Public Power District (NPPD)
| docket = 05000298
| docket = 05000298
| license number = DPR-046
| license number = DPR-046
| contact person = Warnick G G
| contact person = Warnick G
| case reference number = EA-15-089
| case reference number = EA-15-089
| document report number = IR 2016001
| document report number = IR 2016001
Line 19: Line 19:


=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION IV 1600 E. LAMAR BLVD.
{{#Wiki_filter:April 28, 2016


ARLINGTON, TX 76011-4511 April 28, 2016 EA-15-089 Mr. Oscar Vice President
==SUBJECT:==
-Nuclear and CNO Nebraska Public Power District Cooper Nuclear Station 72676 648A Avenue P.O. Box 98 Brownville, NE 68321
COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000298/2016001
 
SUBJECT: COOPER NUCLEAR STATION
- NRC INTEGRATED INSPECTION REPORT 05000 298/2016001


==Dear Mr. Limpias:==
==Dear Mr. Limpias:==
On March 31, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Cooper Nuclear Station.
On March 31, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Cooper Nuclear Station. On April 8, 2016, the NRC inspectors discussed the results of this inspection with you and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.


On April 8, 2016, the NRC inspectors discussed the results of this inspection with you and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.
NRC inspectors documented two findings of very low safety significance (Green) in this report.


NRC inspectors documented two findings of very low safety significance (Green) in this report. Both of these findings involved violations of NRC requirements. The NRC is treating these violations as non
Both of these findings involved violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the NRC Enforcement Policy.
-cited violations (NCVs) consistent with Section 2.3.2.a of the NRC Enforcement Policy.


If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.
If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Cooper Nuclear Station.


Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington
If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the Cooper Nuclear Station.
, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555
-0001; and the NRC resident inspector at the Cooper Nuclear Station
. If you disagree with a cross
-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the Cooper Nuclear Station.


In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, "Public Inspections, Exemptions, Requests for Withholding," a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRC's Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading
In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).
-rm/adams.html (the Public Electronic Reading Room).


Sincerely,/RA/ Gregory G. Warnick, Chief Project Branch C Division of Reactor Projects Docket No
Sincerely,
. 50-298 License No
/RA/  
. DPR-46


===Enclosure:===
Gregory G. Warnick, Chief Project Branch C Division of Reactor Projects
Inspection Report 05000298/2016001 w/


===Attachment:===
Docket No. 50-298 License No. DPR-46
1. Supplemental Information 2. Request for Information for the Occupational/Public Radiation Safety Inspection cc w/ encl: Electronic Distribution


ML16119A44 1 SUNSI Review By: CHY ADAMS Yes No Non-Sensitive Sensitive Publicly Available Non-Publicly Available Keyword: NRC-002 OFFICE SRI:DRP/C RI:DRP/C C:EB1 C:EB2 C:OB C:PSB1 C:PSB2 NAME PVoss CHenderson TFarnholtz GWerner VGaddy MHaire HGepford SIGNATURE
===Enclosure:===
/RA-E/ /RA-E/ /RA/ /RA/ /RA/JKirkland, for /RA/ /RA/ DATE 4/26/16 4/26/16 4/20/16 4/21/16 4/20/16 4/20/16 4/21/16 OFFICE C:DRS/IPAT SPE:DRP/C BC:DRP/C NAME THipschman CYoung GWarnick SIGNATURE
Inspection Report 05000298/2016001 w/ Attachment:
/RA/ /RA/ /RA/ DATE 4/22/16 4/26/16 4/28/16 Letter to Oscar from Greg Warnick dated April 28, 2016
1. Supplemental Information 2. Request for Information for the O


SUBJECT: COOPER NUCLEAR STATION
REGION IV==
- NRC INTEGRATED INSPECTION REPORT 05000 298/2016001 DISTRIBUTION
Docket:
: Regional Administrator (Marc.Dapas@nrc.gov)
05000298 License:
Deputy Regional Administrator (Kriss.Kennedy@nrc.gov)
DPR-46 Report:
DRP Director (Troy.Pruett@nrc.gov)
05000298/2016001 Licensee:
DRP Deputy Director (Ryan.Lantz@nrc.gov
) DRS Director (Anton.Vegel@nrc.gov)
DRS Deputy Director (Jeff.Clark@nrc.gov)
Senior Resident Inspector (Patricia.Voss@nrc.gov) Resident Inspector (Christopher.Henderson@nrc.gov)
Branch Chief, DRP/C (Greg.Warnick@nrc.gov)
Senior Project Engineer (Cale.Young@nrc.gov) Project Engineer (Michael.Stafford@nrc.gov) Project Engineer (Lindsay.Brandt@nrc.gov) Administrative Assistant (Amy.Elam@nrc.gov)
Public Affairs Officer (Victor.Dricks@nrc.gov) Project Manager (Alan.Wang@nrc.gov)
Team Leader, DRS/IPAT (Thomas.Hipschman@nrc.gov)
ACES (R4Enforcement.Resource@nrc.gov)
RITS Coordinator (Marisa.Herrera@nrc.gov
) Regional Counsel (Karla.Fuller@nrc.gov
) Technical Support Assistant (Loretta.Williams@nrc.gov)
Congressional Affairs Officer (Jenny.Weil@nrc.gov)
Congressional Affairs Officer (Angel.Moreno@nrc.gov)
RIV/ETA: OEDO (Jeremy.Bowen@nrc.gov)
ROPreports.Resource@nrc.gov ROPassessment.Resource@nrc.gov Enclosure U.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket: 05000298 License: DPR-46 Report: 05000298/2016001 Licensee:
Nebraska Public Power District Facility:
Nebraska Public Power District Facility:
Cooper Nuclear Station Location:
Cooper Nuclear Station Location:
72676 648A Ave Brownville, NE Dates: January 1 through March 31, 2016 Inspectors:
72676 648A Ave Brownville, NE Dates:
P. Voss, Senior Resident Inspector C. Henderson, Resident Inspector W. Sifre, Senior Reactor Inspector M. Phalen, Senior Health Physicist J. O'Donnell, CHP, Health Physicist Approved By: Greg Warnick Chief, Project Branch C Division of Reactor Projects  
January 1 through March 31, 2016 Inspectors: P. Voss, Senior Resident Inspector C. Henderson, Resident Inspector W. Sifre, Senior Reactor Inspector M. Phalen, Senior Health Physicist J. ODonnell, CHP, Health Physicist Approved By:
Greg Warnick Chief, Project Branch C Division of Reactor Projects  
 
- 2 -


=SUMMARY=
=SUMMARY=
IR 05000298/2016001; 01/01/2016 - 03/31/2016; Cooper Nuclear Station
IR 05000298/2016001; 01/01/2016 - 03/31/2016; Cooper Nuclear Station; Surveillance Testing.
 
; Surveillance Testing
. The inspection activities described in this report were performed between January 1 and March 31, 2016, by the resident inspectors at the Cooper Nuclear Station and inspectors from the NRC's Region IV office
. Two findings of very low safety significance (Green) are documented in this report. Both of these findings involved violations of NRC requirements
. The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red), which is determined using Inspection Manual Chapter 0609, "Significance Determination Process."  Their cross-cutting aspects are determined using Inspection Manual Chapter 0310, "Aspects within the Cross-Cutting Areas."  Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy.


The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG
The inspection activities described in this report were performed between January 1 and March 31, 2016, by the resident inspectors at the Cooper Nuclear Station and inspectors from the NRCs Region IV office. Two findings of very low safety significance (Green) are documented in this report. Both of these findings involved violations of NRC requirements. The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red), which is determined using Inspection Manual Chapter 0609, Significance Determination Process. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310,
-1649, "Reactor Oversight Process."
Aspects within the Cross-Cutting Areas. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.


===Cornerstone: Mitigating Systems===
===Cornerstone: Mitigating Systems===
*
: '''Green.'''
: '''Green.'''
The inspectors identified a non-cited violation of 10 CFR 50.55a, "Codes and Standards," for the licensee's failure to follow the ASME Code for Operation and Maintenance of Nuclear Power Plants when addressing the performance of reactor equipment cooling pump A within the high "required action range" of the inservice testing program. Specifically, on February 11, 2016, the licensee failed to follow ASME Subsection ISTB 6200(b) when engineering personnel, taking corrective action to address pump performance, failed to either correct the cause of the deviation or establish new reference values for the pump. Instead of establishing new reference values, the licensee performed an analysis to administratively raise the upper "required action range" limit, creating a wider range of acceptable pump operation than allowed by Table ISTB-5100-1, "Centrifugal Pump Test Acceptance Criteria.The licensee entered this issue into the corrective action program as Condition Report CR
The inspectors identified a non-cited violation of 10 CFR 50.55a, Codes and Standards, for the licensees failure to follow the ASME Code for Operation and Maintenance of Nuclear Power Plants when addressing the performance of reactor equipment cooling pump A within the high required action range of the inservice testing program. Specifically, on February 11, 2016, the licensee failed to follow ASME Subsection ISTB 6200(b) when engineering personnel, taking corrective action to address pump performance, failed to either correct the cause of the deviation or establish new reference values for the pump. Instead of establishing new reference values, the licensee performed an analysis to administratively raise the upper required action range limit, creating a wider range of acceptable pump operation than allowed by Table ISTB-5100-1, Centrifugal Pump Test Acceptance Criteria. The licensee entered this issue into the corrective action program as Condition Report CR-CNS-2016-00920, took action to reevaluate and rebaseline the pump with new reference values, and performed an extent of condition review to determine if other equipment was impacted by similar interpretations of the code.
-CNS-2016-00920, took action to reevaluate and rebaseline the pump with new reference values, and performed an extent of condition review to determine if other equipment was impacted by similar interpretations of the code.
 
The licensee's failure to establish new reference values for reactor equipment cooling pump A in accordance with the ASME Code was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the human performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the actions initially taken by the licensee would have required a relief request
; could have delayed identification of a degrading pump trend due to the creation of a wider range of acceptable operation; and the licensee's generic interpretation
, that the Table ISTB-5100-1 "acceptable range" could be administratively expanded, represented a programmatic vulnerability.


The inspectors used Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," and determined that the finding had very low safety significance (Green) because it did not represent a design or qualification deficiency, did not represent a loss of safety function for a single train for greater than its technical specification allowed outage time, and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. This finding had a cross-cutting aspect in the area of problem identificatio n and resolution associated with evaluation. Specifically, the licensee failed to thoroughly evaluate performance of reactor equipment cooling pump A in the "required action range" to ensure that the resolution correctly addressed the causes of the degraded performance
The licensees failure to establish new reference values for reactor equipment cooling pump A in accordance with the ASME Code was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the human performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the actions initially taken by the licensee would have required a relief request; could have delayed identification of a degrading pump trend due to the creation of a wider range of acceptable operation; and the licensees generic interpretation, that the Table ISTB-5100-1 acceptable range could be administratively expanded, represented a programmatic vulnerability. The inspectors used Manual Chapter 0609,
[P.2]. (Section 1R22)
Appendix A, The Significance Determination Process (SDP) for Findings At-Power, and determined that the finding had very low safety significance (Green) because it did not represent a design or qualification deficiency, did not represent a loss of safety function for a single train for greater than its technical specification allowed outage time, and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. This finding had a cross-cutting aspect in the area of problem identification and resolution associated with evaluation. Specifically, the licensee failed to thoroughly evaluate performance of reactor equipment cooling pump A in the required action range to ensure that the resolution correctly addressed the causes of the degraded performance [P.2].  
(Section 1R22)  


===Cornerstone: Barrier Integrity===
===Cornerstone: Barrier Integrity===
*
: '''Green.'''
: '''Green.'''
The inspectors identified a non-cited violation of Technical Specification 5.4.1.a, for the licensee's failure to follow Station Procedure 0.26, "Surveillance Program," and assess the operability of high pressure coolant injection steam line isolation instrumentation during surveillance testing. Specifically, the licensee failed to assess the operability of required isolation instrumentation when maintentance personnel opened terminal box 392 during surveillance testing and temporarily invalidated its environmental qualification
The inspectors identified a non-cited violation of Technical Specification 5.4.1.a, for the licensees failure to follow Station Procedure 0.26, Surveillance Program, and assess the operability of high pressure coolant injection steam line isolation instrumentation during surveillance testing. Specifically, the licensee failed to assess the operability of required isolation instrumentation when maintentance personnel opened terminal box 392 during surveillance testing and temporarily invalidated its environmental qualification. Licensee procedures required operations personnel to either establish compensatory measures to restore the terminal box during an event, or declare the instrumentation inoperable and enter the applicable technical specification actions when the terminal box was opened. As an immediate corrective action, the licensee implemented Standing Order 2016-03, which directed operators to establish compensatory measures, if applicable, or declare the affected equipment inoperable when environmentally qualified terminal boxes would be opened during testing. The licensee entered this issue into their corrective action program for resolution as Condition Reports CR-CNS-2016-00320 and CR-CNS-2016-00476.
. Licensee procedures required operations personnel to either establish compensatory measure s to restore the terminal box during an event
, or declare the instrumentation inoperable and enter the applicable technical specification actions when the terminal box was opened
. As an immediate corrective action
, the licensee implement ed Standing Order 2016-03, which directed operators to establish compensatory measures, if applicable, or declare the affected equipment inoperable when environmentally qualified terminal boxes would be opened during testing. The licensee entered this issue into their corrective action program for resolution as Condition Reports CR
-CNS-2016-00320 and CR
-CNS-2016-00476. The licensee's failure to assess the operability of high pressure coolant injection instrumentation when the associated terminal box was opened during surveillance testing, in violation of Station Procedure 0.26, was a performance deficiency.


The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the structure, system, component, and barrier performance attribute of the Barrier Integrity Cornerstone, and adversely affected the cornerstone objective to ensure the radiological barrier functionality of containment isolation. Specifically, with terminal box 392 open, its environmental qualification was temporarily invalidated, making the high pressure coolant injection low steam pressure and high steam flow containment isolation instrumentation inoperable during surveillance testing. In addition, two other terminal boxes and their associated surveillances were impacted by the performance deficiency. Using Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At-Power," the inspectors determined that the finding had very low safety significance (Green) because it: (1) did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components; and (2)did not involve an actual reduction in function of hydrogen igniters in the reactor containment. The finding had a cross-cutting aspect in the area of human performance associated with work management. Specifically, the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority, including the identification and management of risk commensurate with opening terminal box 392 during surveillance testing
The licensees failure to assess the operability of high pressure coolant injection instrumentation when the associated terminal box was opened during surveillance testing, in violation of Station Procedure 0.26, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the structure, system, component, and barrier performance attribute of the Barrier Integrity Cornerstone, and adversely affected the cornerstone objective to ensure the radiological barrier functionality of containment isolation. Specifically, with terminal box 392 open, its environmental qualification was temporarily invalidated, making the high pressure coolant injection low steam pressure and high steam flow containment isolation instrumentation inoperable during surveillance testing. In addition, two other terminal boxes and their associated surveillances were impacted by the performance deficiency. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, the inspectors determined that the finding had very low safety significance (Green) because it: (1) did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components; and (2) did not involve an actual reduction in function of hydrogen igniters in the reactor containment. The finding had a cross-cutting aspect in the area of human performance associated with work management. Specifically, the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority, including the identification and management of risk commensurate with opening terminal box 392 during surveillance testing [H.5].  
[H.5]. (Section 1R22)  
(Section 1R22)


==PLANT STATUS==
=PLANT STATUS=
The Cooper Nuclear Station began the inspection period at full power. On February 12, 2016, the licensee lowered reactor power to approximately 70 percent in order to perform surveillance testing and planned work on reactor feedwater pump B. The plant returned to full power on February 13, 2016, where it remained for the rest of the reporting period, ex cept for minor reductions in power to support scheduled surveillance testing and rod pattern adjustments
.


=REPORT DETAILS=
The Cooper Nuclear Station began the inspection period at full power. On February 12, 2016, the licensee lowered reactor power to approximately 70 percent in order to perform surveillance testing and planned work on reactor feedwater pump B. The plant returned to full power on February 13, 2016, where it remained for the rest of the reporting period, except for minor reductions in power to support scheduled surveillance testing and rod pattern adjustments.
 
REPORT DETAILS


==REACTOR SAFETY==
==REACTOR SAFETY==
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity
Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity {{a|1R04}}
{{a|1R04}}
 
==1R04 Equipment Alignment==
==1R04 Equipment Alignment==
{{IP sample|IP=IP 71111.04}}
{{IP sample|IP=IP 71111.04}}
===.1 Partial Walk===


down
===.1 Partial Walkdown===
====a. Inspection Scope====
The inspectors performed partial system walkdowns of the following risk-significant systems:
* January 17, 2016, High pressure coolant injection steam isolation instrumentation and control system for valves HPCI-MOV-15 and HPCI-MOV-16
* February 19, 2016, Service water cross connect valves SW-MOV-36 and SW-MOV-37 and design flow requirements
* February 29, 2016, Diesel generator sequential loading and kW loading analysis
* March 23, 2016, Instrument air system and reactor equipment cooling The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.


====a. Inspection Scope====
These activities constituted four partial system walkdown samples, as defined in Inspection Procedure 71111.04.
The inspectors performed partial system walkdowns of the following risk
-significant systems:  January 17, 2016, High pressure coolant injection steam isolation instrumentation and control system for valves HPCI-MOV-15 and HPCI-MOV-16  February 19, 2016, Service water cross connect valves SW
-MOV-36 and SW-MOV-37 and design flow requirement s  February 29, 2016, Diesel generator sequential loading and kW loading analysis March 23, 2016, Instrument air system and reactor equipment cooling The inspectors reviewed the licensee's procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration
. These activities constitute d four partial system walkdown samples, as defined in Inspection Procedure 71111.04.


====b. Findings====
====b. Findings====
Line 147: Line 110:


===.2 Complete Walkdown===
===.2 Complete Walkdown===
====a. Inspection Scope====
====a. Inspection Scope====
On March 8, 2016, the inspectors performed a complete system walkdown inspection of the residual heat removal service water system
On March 8, 2016, the inspectors performed a complete system walkdown inspection of the residual heat removal service water system. The inspectors reviewed the licensees procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, open condition reports, in-process design changes, temporary modifications, and other open items tracked by the licensees operations and engineering departments. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.
. The inspectors reviewed the licensee's procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, open condition reports, in
-process design changes, temporary modifications, and other open items tracked by the licensee's operations and engineering departments
. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.


These activities constitute d one complete system walkdown sample
These activities constituted one complete system walkdown sample, as defined in Inspection Procedure 71111.04.
, as defined in Inspection Procedure 71111.04.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R05}}
{{a|1R05}}
 
==1R05 Fire Protection==
==1R05 Fire Protection==
{{IP sample|IP=IP 71111.05}}
{{IP sample|IP=IP 71111.05}}
Line 165: Line 123:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the licensee's fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety
The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:
January 11, 2016, Reactor feed pump s area, Fire Area TB-A, Zone 11E February 24, 2016, Diesel generator room 1, Fire Area DG-A, Zone 14A and 14C February 24, 2016, Diesel generator room 2, Fire Area DG
* January 11, 2016, Reactor feed pumps area, Fire Area TB-A, Zone 11E
-B, Zone 14B and 14D March 3, 2016, Auxiliary relay room, Fire Area CB-D, Zone 8A For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensee's fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.
* February 24, 2016, Diesel generator room 1, Fire Area DG-A, Zone 14A and 14C
* February 24, 2016, Diesel generator room 2, Fire Area DG-B, Zone 14B and 14D
* March 3, 2016, Auxiliary relay room, Fire Area CB-D, Zone 8A  


These activities constitute d four quarterly inspection sample s, as defined in Inspection Procedure 71111.05.
For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.
 
These activities constituted four quarterly inspection samples, as defined in Inspection Procedure 71111.05.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R06}}
{{a|1R06}}
 
==1R06 Flood Protection Measures==
==1R06 Flood Protection Measures==
{{IP sample|IP=IP 71111.06}}
{{IP sample|IP=IP 71111.06}}


====a. Inspection Scope====
====a. Inspection Scope====
On February 29, 2016, the inspectors completed an inspection of the station's ability to mitigate flooding due to internal causes. After reviewing the licensee's flooding analysis, the inspectors chose one plant area containing risk-significant structures, systems, and components that were susceptible to flooding:
On February 29, 2016, the inspectors completed an inspection of the stations ability to mitigate flooding due to internal causes. After reviewing the licensees flooding analysis, the inspectors chose one plant area containing risk-significant structures, systems, and components that were susceptible to flooding:
Control building basement The inspectors reviewed plant design features and licensee procedures for coping with internal flooding. The inspectors walked down the selected area to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.
* Control building basement The inspectors reviewed plant design features and licensee procedures for coping with internal flooding. The inspectors walked down the selected area to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.


These activities constitute d completion of one flood protection measures sample, as defined in Inspection Procedure 71111.06.
These activities constituted completion of one flood protection measures sample, as defined in Inspection Procedure 71111.06.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R11}}
{{a|1R11}}
 
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
==1R11 Licensed Operator Requalification Program and Licensed Operator Performance==
{{IP sample|IP=IP 71111.11}}
{{IP sample|IP=IP 71111.11}}
===.1 Review of Licensed Operator Requalification===
===.1 Review of Licensed Operator Requalification===
====a. Inspection Scope====
On February 19, 2016, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities.


====a. Inspection Scope====
These activities constituted completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.
On February 19, 2016, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators' critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities
. These activities constitute d completion of one quarterly licensed operator requalification program sample
, as defined in Inspection Procedure 71111.11.


====b. Findings====
====b. Findings====
Line 199: Line 161:


===.2 Review of Licensed Operator Performance===
===.2 Review of Licensed Operator Performance===
====a. Inspection Scope====
On February 13, 2016, the inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened activity due to maintenance and testing associated with a planned downpower to 70 percent. The inspectors observed the operators performance of the following activities:
* Rod manipulations associated with the downpower and rod pattern change, including the pre-job brief
* Main steam isolation valve closure reactor protection system surveillance testing, including the pre-job brief


====a. Inspection Scope====
In addition, the inspectors assessed the operators adherence to plant procedures, including conduct of operations procedure and other operations department policies.
On February 13, 2016, the inspectors observed the performance of on-shift licensed operators in the plant's main control room. At the time of the observations, the plant was in a period of heightened activity due to maintenance and testing associated with a planned downpower to 70 percent. The inspectors observed the operators' performance of the following activities:
Rod manipulations associated with the downpower and rod pattern change
, including the pre
-job brief Main steam isolation valve closure reactor protection system surveillance testing, including the pre-job brief In addition, the inspectors assessed the operators' adherence to plant procedures, including conduct of operations procedure and other operations department policies.


These activities constitute d completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.
These activities constituted completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R12}}
{{a|1R12}}
 
==1R12 Maintenance Effectiveness==
==1R12 Maintenance Effectiveness==
{{IP sample|IP=IP 71111.12}}
{{IP sample|IP=IP 71111.12}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed two instances of degraded performance or condition of safety-related or risk-significant structures, systems, and components (SSCs):   February 29, 2016, Core spray reference leg injection January 19, 2016
The inspectors reviewed two instances of degraded performance or condition of safety-related or risk-significant structures, systems, and components (SSCs):
, Reactor recirculation motor generator sets
* February 29, 2016, Core spray reference leg injection
* January 19, 2016, Reactor recirculation motor generator sets  


The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensee's corrective actions. The inspectors reviewed the licensee's work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensee's characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.
The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.


These activities constitute d completion of two maintenance effectiveness samples
These activities constituted completion of two maintenance effectiveness samples, as defined in Inspection Procedure 71111.12.
, as defined in Inspection Procedure 71111.12.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R13}}
{{a|1R13}}
 
==1R13 Maintenance Risk Assessments and Emergent Work Control==
==1R13 Maintenance Risk Assessments and Emergent Work Control==
{{IP sample|IP=IP 71111.13}}
{{IP sample|IP=IP 71111.13}}
Line 231: Line 193:
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:
February 3, 2016, Residual heat removal service water system maintenance window, Division II February 13, 2016, Feedwater pump B repair during planned downpower March 17, 2016, Reactor core isolation cooling maintenance window and northeast quad fan coil replacement March 25, 2016, Diesel generator system maintenance window, Division II The inspectors verified that these risk assessment s were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensee's risk assessments and verified that the licensee implemented appropriate risk management actions based on the result of the assessments.
* February 3, 2016, Residual heat removal service water system maintenance window, Division II
* February 13, 2016, Feedwater pump B repair during planned downpower
* March 17, 2016, Reactor core isolation cooling maintenance window and northeast quad fan coil replacement
* March 25, 2016, Diesel generator system maintenance window, Division II The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the result of the assessments.


The inspectors also observed portions of two emergent work activities that had the potential to affect the functional capability of mitigating systems or to impact barrier integrity:
The inspectors also observed portions of two emergent work activities that had the potential to affect the functional capability of mitigating systems or to impact barrier integrity:
January 19, 2016, Diesel generator 1 repairs due to frequency starting time greater than technical specification surveillance requirements January 29, 2016, Loss of plant monitoring and information system/Gardel power supplies The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected structures, systems, and components.
* January 19, 2016, Diesel generator 1 repairs due to frequency starting time greater than technical specification surveillance requirements
* January 29, 2016, Loss of plant monitoring and information system/Gardel power supplies The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected structures, systems, and components.


These activities constitute d completion of six maintenance risk assessment and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.
These activities constituted completion of six maintenance risk assessment and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R15}}
{{a|1R15}}
==1R15 Operability Determinations==


and Functionality Assessments (71111.15)
==1R15 Operability Determinations and Functionality Assessments==
{{IP sample|IP=IP 71111.15}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed five operability determinations that the licensee performed for degraded or nonconforming structures, systems, or components (SSCs):
The inspectors reviewed five operability determinations that the licensee performed for degraded or nonconforming structures, systems, or components (SSCs):
January 15, 2016
* January 15, 2016, Operability determination of a control rod drive scram outlet valve due to leakage, CR-CNS-2016-0075
, Operability determination of a control rod drive scram outlet valve due to leakage, CR-CNS-2016-0075 January 17, 2016, Operability determination of service water when the idle diesel generator is not isolated for a loss of offsite power/loss of coolant accident, CR-CNS-2016-00201 January 22, 2016
* January 17, 2016, Operability determination of service water when the idle diesel generator is not isolated for a loss of offsite power/loss of coolant accident, CR-CNS-2016-00201
, Operability determination of the 125V Battery A due to lifting positive battery posts, CR
* January 22, 2016, Operability determination of the 125V Battery A due to lifting positive battery posts, CR-CNS-2015-06703
-CNS-2015-06703 March 16, 2016, Operability determination of reactor equipment cooling pump A due to exceedance of inservice testing required action limits, CR-CNS-2016-00784 March 25, 2016, Operability determination of service water due to inconsistent pump column minimum wall thickness acceptance criteria, CR-CNS-2016-01448 The inspectors reviewed the timeliness and technical adequacy of the licensee's evaluations. Where the licensee determined the degraded SSC to be operable, t he inspectors verified that the licensee's compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC
* March 16, 2016, Operability determination of reactor equipment cooling pump A due to exceedance of inservice testing required action limits, CR-CNS-2016-00784
.
* March 25, 2016, Operability determination of service water due to inconsistent pump column minimum wall thickness acceptance criteria, CR-CNS-2016-01448 The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.
On January 25, 2016, the inspectors completed their review of operator actions taken or planned to compensate for degraded or nonconforming conditions.


The inspectors verified that the licensee effectively managed these operator workarounds to prevent adverse effects on the function of mitigating systems and to minimize their impact on the operators' ability to implement abnormal and emergency operating procedures.
On January 25, 2016, the inspectors completed their review of operator actions taken or planned to compensate for degraded or nonconforming conditions. The inspectors verified that the licensee effectively managed these operator workarounds to prevent adverse effects on the function of mitigating systems and to minimize their impact on the operators ability to implement abnormal and emergency operating procedures.


These activities constituted completion of six operability and functionality review samples, which included one operator work
These activities constituted completion of six operability and functionality review samples, which included one operator work-around sample, as defined in Inspection Procedure 71111.15.
-around sample, as defined in Inspection Procedure 71111.15.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R18}}
{{a|1R18}}
 
==1R18 Plant Modifications==
==1R18 Plant Modifications==
{{IP sample|IP=IP 71111.18}}
{{IP sample|IP=IP 71111.18}}


====a. Inspection Scope====
====a. Inspection Scope====
On March 9, 2016, the inspectors reviewed a permanent plant modification associated with the replacement of safety-related General Electric magne blast breakers with Siemens horizontal vacuum bottle circuit breakers which affected risk
On March 9, 2016, the inspectors reviewed a permanent plant modification associated with the replacement of safety-related General Electric magne blast breakers with Siemens horizontal vacuum bottle circuit breakers which affected risk-significant structures, systems, and components (SSCs).
-significant structures, systems, and components (SSCs)
 
.
The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post-modification testing was adequate to establish the operability of the SSCs as modified.
The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post
-modification testing was adequate to establish the operability of the SSC s as modified.


These activities constitute d completion of one sample of permanent modifications
These activities constituted completion of one sample of permanent modifications, as defined in Inspection Procedure 71111.18.
, as defined in Inspection Procedure 71111.18.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R19}}
{{a|1R19}}
==1R19 Post-Maintenance==


Testing (71111.19)
==1R19 Post-Maintenance Testing==
{{IP sample|IP=IP 71111.19}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed six post-maintenance testing activities that affected risk
The inspectors reviewed six post-maintenance testing activities that affected risk-significant structures, systems, or components (SSCs):
-significant structures, systems, or components (SSCs):
* January 19, 2016, Diesel generator 1 emergent work
January 19, 2016, Diesel generator 1 emergent work February 3, 2016, Residual heat removal pump B relay and breaker maintenance February 3, 2016, Residual heat removal service water booster pump B discharge valve work February 3, 2016, Residual heat removal service water pump D outboard mechanical seal and discharge check valve inspection February 19, 2016, Residual heat removal and residual heat removal service water motor operated valve maintenance, Division II February 19, 2016, Torus to reactor vacuum breaker control switch replacement The inspectors reviewed licensing- and design
* February 3, 2016, Residual heat removal pump B relay and breaker maintenance
-basis documents for the SSCs and the maintenance and post-maintenance test procedures.
* February 3, 2016, Residual heat removal service water booster pump B discharge valve work
* February 3, 2016, Residual heat removal service water pump D outboard mechanical seal and discharge check valve inspection
* February 19, 2016, Residual heat removal and residual heat removal service water motor operated valve maintenance, Division II
* February 19, 2016, Torus to reactor vacuum breaker control switch replacement The inspectors reviewed licensing-and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.


The inspectors observed the performance of the post
These activities constituted completion of six post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.
-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs
.
These activities constitute d completion of six post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|1R22}}
{{a|1R22}}
 
==1R22 Surveillance Testing==
==1R22 Surveillance Testing==
{{IP sample|IP=IP 71111.22}}
{{IP sample|IP=IP 71111.22}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the structures, systems, and components (SSCs) were capable of performing their safety functions:
The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the structures, systems, and components (SSCs) were capable of performing their safety functions:  
In-service test s: January 25, 2016, High pressure coolant injection quarterly inservice test surveillance Other surveillance tests:
 
January 14, 2016, High pressure coolant injection steam isolation valves HPCI-MOV-15 and HPCI-MOV-16 surveillance testing for primary containment isolation for the steam line break January 26, 2016, Service water quarterly and post
In-service tests:
-loss of coolant accident flow surveillance acceptance criteria February 9, 2016, Diesel generator 31 day operability test, Division I February 19, 2016, Reactor equipment cooling pump A inservice testing surveillance March 3, 2016, SW
* January 25, 2016, High pressure coolant injection quarterly inservice test surveillance Other surveillance tests:
-MOV-36 and SW
* January 14, 2016, High pressure coolant injection steam isolation valves HPCI-MOV-15 and HPCI-MOV-16 surveillance testing for primary containment isolation for the steam line break
-MOV-37 surveillance testing The inspectors verified that these test s met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the tests satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.
* January 26, 2016, Service water quarterly and post-loss of coolant accident flow surveillance acceptance criteria
* February 9, 2016, Diesel generator 31 day operability test, Division I
* February 19, 2016, Reactor equipment cooling pump A inservice testing surveillance
* March 3, 2016, SW-MOV-36 and SW-MOV-37 surveillance testing The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the tests satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.


These activities constitute d completion of six surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.
These activities constituted completion of six surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.


====b. Findings====
====b. Findings====
(1) Failure to Follow ASME Code Requirements when taking Corrective Actions for a Pump in the Required Action Range Introduction
: (1) Failure to Follow ASME Code Requirements when taking Corrective Actions for a Pump in the Required Action Range  
. The inspectors identified a Green, non-cited violation of 10 CFR 50.55a, "Codes and Standards," for the licensee's failure to follow the ASME Code for Operation and Maintenance of Nuclear Power Plants (OM) when addressing the performance of reactor equipment cooling (REC) pump A within the high "required action range" of the inservice testing program. Specifically, the licensee failed to follow ASME Subsection ISTB-6200(b) when engineering personnel, while taking corrective action to address pump performance, failed to either correct the cause of the deviation or establish new reference values for the pump.


Description
=====Introduction.=====
. On February 11, 2016, the licensee performed Surveillance Procedure 6.1REC.101, "REC Surveillance Operation (IST)
The inspectors identified a Green, non-cited violation of 10 CFR 50.55a, Codes and Standards, for the licensees failure to follow the ASME Code for Operation and Maintenance of Nuclear Power Plants (OM) when addressing the performance of reactor equipment cooling (REC) pump A within the high required action range of the inservice testing program. Specifically, the licensee failed to follow ASME Subsection ISTB-6200(b) when engineering personnel, while taking corrective action to address pump performance, failed to either correct the cause of the deviation or establish new reference values for the pump.
- Div 1," for the two
-year comprehensive inservice test (IST) of REC pump A. This procedure was being used to meet the IST requirements for the pump in accordance with the 2001 Edition through the 2003 Addenda of the ASME OM Code. During the IST, the pump exceeded the upper limit for discharge pressure required by the test, which put the pump in the high "required action range" in accordance with the ASME Code. Consistent with the surveillance procedure and ASME OM Subsection IST B-6200(b), the licensee declared the pump inoperable upon discovery of the condition. The licensee initiated condition report CR
-CNS-2016-00784 to document the unacceptable inservice test results for REC pump A. ASME Section ISTB
-6200, "Corrective Action," Subsection (b), states, "If the measured test parameter values fall within the "required action range" of Table ISTB
-5100-1, the pump shall be declared inoperable until either the cause of the deviation has been determined and the condition is corrected, or an analysis of the pump is performed and new reference values are established in accordance with ISTB
-6200(c)."  The licensee determined that the pump was operating acceptably, and as a result, determined that there was no need to correct the cause of the deviation in pump performance. However, the licensee did not establish new reference values, which serve to provide a baseline of acceptable pump performance, in accordance with ISTB
-6200(c). Instead, engineering personnel performed an analysis which assessed the operational readiness of the pump and evaluated pump performance trends as discussed in ISTB
-6200(c), but rather than rebaseline the pump, the licensee administratively raised the upper "required action" limit. Following this action, operations personnel declared REC pump A operable.


The inspectors reviewed the licensee's actions and challenged the site's decision to neither correct nor rebaseline the pump in accordance with Subsection ISTB
=====Description.=====
-6200(b). The inspectors observed that the licensee's actions to raise the upper "required action" limit inappropriately created a wider range of acceptable pump operation than allowed by ASME Table ISTB
On February 11, 2016, the licensee performed Surveillance Procedure 6.1REC.101, REC Surveillance Operation (IST) - Div 1, for the two-year comprehensive inservice test (IST) of REC pump A. This procedure was being used to meet the IST requirements for the pump in accordance with the 2001 Edition through the 2003 Addenda of the ASME OM Code. During the IST, the pump exceeded the upper limit for discharge pressure required by the test, which put the pump in the high required action range in accordance with the ASME Code. Consistent with the surveillance procedure and ASME OM Subsection ISTB-6200(b), the licensee declared the pump inoperable upon discovery of the condition. The licensee initiated condition report CR-CNS-2016-00784 to document the unacceptable inservice test results for REC pump A.
-5100-1, "Centrifugal Pump Test Acceptance Criteria."  In consultation with NRC regional and headquarters ASME Code experts, the inspectors concluded that these actions put the site in nonconformance with the ASME Code. The inspectors observed that the licensee's change would have required an NRC relief request and could have delayed identification of a degrading pump trend due to the creation of a wider range of acceptable operation. In response to inspector questions, the licensee determined that they had used this same method for different equipment on previous occasions
. The inspectors determined that the licensee's generic interpretation that Table ISTB
-5100-1 acceptance criteria multipliers could be changed using Subsection ISTB-6200 represented a potential programmatic vulnerability.


This issue was entered into the licensee's corrective action program as CR
ASME Section ISTB-6200, Corrective Action, Subsection (b), states, If the measured test parameter values fall within the required action range of Table ISTB-5100-1, the pump shall be declared inoperable until either the cause of the deviation has been determined and the condition is corrected, or an analysis of the pump is performed and new reference values are established in accordance with ISTB-6200(c). The licensee determined that the pump was operating acceptably, and as a result, determined that there was no need to correct the cause of the deviation in pump performance. However, the licensee did not establish new reference values, which serve to provide a baseline of acceptable pump performance, in accordance with ISTB-6200(c). Instead, engineering personnel performed an analysis which assessed the operational readiness of the pump and evaluated pump performance trends as discussed in ISTB-6200(c), but rather than rebaseline the pump, the licensee administratively raised the upper required action limit. Following this action, operations personnel declared REC pump A operable.
-CNS-2016-00920, and the licensee subsequently took corrective action to establish new reference values for the pump
 
.  
The inspectors reviewed the licensees actions and challenged the sites decision to neither correct nor rebaseline the pump in accordance with Subsection ISTB-6200(b).
 
The inspectors observed that the licensees actions to raise the upper required action limit inappropriately created a wider range of acceptable pump operation than allowed by ASME Table ISTB-5100-1, Centrifugal Pump Test Acceptance Criteria. In consultation with NRC regional and headquarters ASME Code experts, the inspectors concluded that these actions put the site in nonconformance with the ASME Code. The inspectors observed that the licensees change would have required an NRC relief request and could have delayed identification of a degrading pump trend due to the creation of a wider range of acceptable operation. In response to inspector questions, the licensee determined that they had used this same method for different equipment on previous occasions. The inspectors determined that the licensees generic interpretation that Table ISTB-5100-1 acceptance criteria multipliers could be changed using Subsection ISTB-6200 represented a potential programmatic vulnerability. This issue was entered into the licensees corrective action program as CR-CNS-2016-00920, and the licensee subsequently took corrective action to establish new reference values for the pump.


=====Analysis.=====
=====Analysis.=====
The licensee's failure to establish new reference values for REC pump A in accordance with the ASME OM code was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the human performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the actions initially taken by the licensee would have required a relief request
The licensees failure to establish new reference values for REC pump A in accordance with the ASME OM code was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the human performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the actions initially taken by the licensee would have required a relief request; could have delayed identification of a degrading pump trend due to the creation of a wider range of acceptable operation; and the licensees generic interpretation that the Table ISTB-5100-1 acceptable range could be administratively expanded represented a programmatic vulnerability. The inspectors used Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, and determined that the finding had very low safety significance (Green) because it did not represent a design or qualification deficiency, did not represent a loss of safety function for a single train for greater than its technical specification allowed outage time, and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. This finding had a cross-cutting aspect in the area of problem identification and resolution associated with evaluation. Specifically, the licensee failed to thoroughly evaluate performance of REC pump A in the required action range to ensure that the resolution correctly addressed the causes of the degraded performance [P.2].  
; could have delayed identification of a degrading pump trend due to the creation of a wider range of acceptable operation; and the licensee's generic interpretation that the Table ISTB
-5100-1 "acceptable range" could be administratively expanded represented a programmatic vulnerability.


The inspectors used Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At
=====Enforcement.=====
-Power," dated June 19, 2012, and determined that the finding had very low safety significance (Green) because it did not represent a design or qualification deficiency, did not represent a loss of safety function for a single train for greater than its technical specification allowed outage time, and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. This finding had a cross-cutting aspect in the area of problem identificatio n and resolution associated with evaluation.
Title 10 of the Code of Federal Regulations, Section 50.55a(b), Codes and Standards, requires, in part, that systems and components of boiling and pressurized water cooled nuclear power reactors must meet the requirements of the ASME Code for Operation and Maintenance of Nuclear Power Plants. Contrary to the above, on February 11, 2016, the licensee failed to ensure that systems and components in the plant met the requirements of the ASME OM Code. Specifically, the licensee failed to ensure ASME Subsection ISTB 6200(b) was met when engineering personnel, while taking corrective action to address REC pump A performance, failed to either correct the cause of the deviation or establish new reference values for the pump.


Specifically, the licensee failed to thoroughly evaluate performance of REC pump A in the "required action range" to ensure that the resolution correctly addressed the causes of the degraded performance
Upon discovery, the licensee took action to reevaluate and rebaseline the pump with new reference values, and performed an extent of condition review to determine if other equipment was impacted by similar interpretations of the code. This violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy, because it was of very low safety significance (Green) and was entered into the licensees corrective action program as Condition Report CR-CNS-2016-00920.
[P.2]. Enforcement
. Title 10 of the Code of Federal Regulations, Section 50.55a(b), "Codes and Standards," requires, in part, that systems and components of boiling and pressurized water cooled nuclear power reactors must meet the requirements of the ASME Code for Operation and Maintenance of Nuclear Power Plants.


Contrary to the above, on February 11, 2016, the licensee failed to ensure that systems and components in the plant met the requirements of the ASME OM Code. Specifically, the licensee failed to ensure ASME Subsection ISTB 6200(b) was met when engineering personnel, while taking corrective action to address REC pump A performance, failed to either correct the cause of the deviation or establish new reference values for the pump. Upon discovery, the licensee took action to reevaluate and rebaseline the pump with new reference values, and performed an extent of condition review to determine if other equipment was impacted by similar interpretations of the code
(NCV 05000298/2016001-01, Failure to Follow ASME Code Requirements when taking Corrective Actions for a Pump in the Required Action Range)
. This violation is being treated as a non
: (2) Failure to Assess Operability of Technical Specification System Functions during Surveillance Testing  
-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy, because it was of very low safety significance (Green) and was entered into the licensee's corrective action program as Condition Report CR
-CNS-2016-00920.  (NCV 05000298/2016001
-01, "Failure to Follow ASME Code Requirements when taking Corrective Actions for a Pump in the Required Action Range
")  (2) Failure to Assess Operability of Technical Specification System Functions during Surveillance Testing


=====Introduction.=====
=====Introduction.=====
The inspectors identified a Green, non
The inspectors identified a Green, non-cited violation of Technical Specification (TS) 5.4.1.a, for the licensees failure to follow Station Procedure 0.26, Surveillance Program, and assess the operability of high pressure coolant injection (HPCI) steam line isolation instrumentation during surveillance testing. Specifically, the licensee failed to assess the operability of required HPCI isolation instrumentation when maintenance personnel opened terminal box (TB) 392 during surveillance testing and temporarily invalidated its environmental qualification.
-cited violation of Technical Specification (TS) 5.4.1.a, for the licensee's failure to follow Station Procedure 0.26, "Surveillance Program," and assess the operability of high pressure coolant injection (HPCI) steam line isolation instrumentation during surveillance testing. Specifically, the licensee failed to assess the operability of required HPCI isolation instrumentation when maintenance personnel opened terminal box (TB) 392 during surveillance testing and temporarily invalidated its environmental qualification.


=====Description.=====
=====Description.=====
On January 14, 2016, the inspectors observed surveillance testing for the Division 1 HPCI low steam pressure containment isolation function for HPCI
On January 14, 2016, the inspectors observed surveillance testing for the Division 1 HPCI low steam pressure containment isolation function for HPCI-MOV-15 in accordance with Station Procedure 6.1HPCI.701, HPCI Steam Line Low Pressure Channel Functional Test (DIV 1), Revision 5, under Work Order 5022860. During the surveillance test the inspectors identified that the licensee opened TB 392 to conduct the surveillance test. This terminal box was identified as environmentally qualified (EQ).
-MOV-15 in accordance with Station Procedure 6.1HPCI.701, "HPCI Steam Line Low Pressure Channel Functional Test (DIV 1)," Revision 5, under Work Order 5022860. During the surveillance test the inspectors identified that the licensee opened TB 392 to conduct the surveillance test
. This terminal box was identified as environmentally qualified (
EQ). The inspectors questioned if TB 392 was EQ in the open condition during the surveillance test.


Following a review of documentation for the terminal box, the inspectors determined that TB 392 was only EQ in the closed condition in accordance with drawing CNS
The inspectors questioned if TB 392 was EQ in the open condition during the surveillance test. Following a review of documentation for the terminal box, the inspectors determined that TB 392 was only EQ in the closed condition in accordance with drawing CNS-EQ-122, Sheet 1 and Sheet 2, Cooper Nuclear Station EQ Configuration Detail Terminal Boxes and Equipment Enclosures, Revision 6 and Revision 5. Drawing CNS-EQ-122, Sheet 1 and Sheet 2, stated that the enclosure for TB 392 was credited with protecting terminal blocks from direct exposure to high-energy line break (HELB) conditions and did not contain the field wires and Raychem splices that would allow the instrumentation to be EQ without an enclosure.
-EQ-122, Sheet 1 and Sheet 2, "Cooper Nuclear Station EQ Configuration Detail Terminal Boxes and Equipment Enclosures," Revision 6 and Revision 5. Drawing CNS-EQ-122, Sheet 1 and Sheet 2, stated that the enclosure for TB 392 was credited with protecting terminal blocks from direct exposure to high
-energy line break (HELB) conditions and did not contain the field wires and Raychem splices that would allow the instrumentation to be EQ without an enclosure.


Station Procedure 0.26, "Surveillance Program," Revision 68, Section 5 and Discussion Section 1.6 required the licensee to assess operability of TS system functions during surveillance testing
Station Procedure 0.26, Surveillance Program, Revision 68, Section 5 and Discussion Section 1.6 required the licensee to assess operability of TS system functions during surveillance testing, and stated that delayed entry was only allowed if there was not a loss of function. Section 5 of this procedure stated, the Shift Manager shall: be aware of any other systems affected by the test and how they are affected. Discussion Section 1.6 stated, TS requirements may have notes that allow delayed entry into conditions and required actions for equipment made inoperable by performance of the surveillance. Even though delayed entry is allowed, the equipment/component is still considered inoperable while performing these surveillances. The delayed entry is only allowed if there is not a loss of function. Additionally, Station Procedure 0-Barrier, Barrier Control Process, Revision 21, stated that opening terminal boxes in the reactor building required that either a compensatory measure be put in place or the SSC be declared inoperable.
, and stated that delayed entry was only allowed if there was not a loss of function. Section 5 of this procedure stated, the "Shift Manager shall:
be aware of any other systems affected by the test and how they are affected
.Discussion Section 1.6 state d, "TS requirements may have notes that allow delayed entry into conditions and required actions for equipment made inoperable by performance of the surveillance. Even though delayed entry is allowed, the equipment/component is still considered inoperable while performing these surveillances. The delayed entry is only allowed if there is not a loss of function.Additionally, Station Procedure 0-Barrier, "Barrier Control Process," Revision 21, stated that opening terminal boxes in the reactor building required that either a compensatory measure be put in place or the SSC be declared inoperable.


The station did not implement a compensatory measure or declare instrumentation in the TB inoperable.
The station did not implement a compensatory measure or declare instrumentation in the TB inoperable. The inspectors and licensee concluded that the shift manager should have been aware of the impacts of opening the TB, and in accordance with procedures, should have declared the TS system function inoperable for the HPCI low steam pressure and HPCI high steam flow isolation instrumentation when TB 392 was opened.


The inspectors and licensee concluded that the shift manager should have been aware of the impacts of opening the TB, and in accordance with procedures, should have declared the TS system function inoperable for the HPCI low steam pressure and HPCI high steam flow isolation instrumentation when TB 392 was opened. Therefore, usage of the six hour delayed entry time for TS 3.3.6.1, "Primary Containment Isolation Instruments," was not allowed per Procedure 0.26 due to the instruments not being inoperable solely for surveillance testing.
Therefore, usage of the six hour delayed entry time for TS 3.3.6.1, Primary Containment Isolation Instruments, was not allowed per Procedure 0.26 due to the instruments not being inoperable solely for surveillance testing. As immediate corrective actions, the licensee identified additional TBs impacted by this concern, and implemented Standing Order 2016-03, which directed operators to either establish compensatory measures or declare the affected equipment inoperable when EQ TBs would be opened during testing. The licensee created long term corrective actions to assess whether compensatory measures could be justified for TBs opened during surveillance testing in the reactor building, to assess whether open TBs could be qualified, and to update station procedures as required. The license entered this deficiency into their corrective action program for resolution as Condition Reports CR-CNS-2016-00320 and CR-CNS-2016-00476.
 
As immediate corrective action s, the licensee identified additional TBs impacted by this concern, and implemented Standing Order 2016-03, which directed operators to either establish compensatory measures or declare the affected equipment inoperable when EQ TBs would be opened during testing. The licensee created long term corrective action s to assess whether compensatory measures could be justified for TBs opened during surveillance testing in the reactor building
, to assess whether open TBs could be qualified, and to update station procedures as required. The license entered this deficiency into their corrective action program for resolution as Condition Reports CR
-CNS-2016-00320 and CR-CNS-2016-00476.  


=====Analysis.=====
=====Analysis.=====
The licensee's failure to assess the operability of HPCI isolation instrumentation when the associated terminal box was opened during surveillance testing, in violation of Station Procedure 0.26, was a performance deficiency.
The licensees failure to assess the operability of HPCI isolation instrumentation when the associated terminal box was opened during surveillance testing, in violation of Station Procedure 0.26, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the SSC and barrier performance attribute of the Barrier Integrity Cornerstone, and adversely affected the cornerstone objective to ensure the radiological barrier functionality of containment isolation. Specifically, with terminal box 392 open, its environmental qualification was temporarily invalidated, making the HPCI isolation instrumentation inoperable during surveillance testing. In addition, two other terminal boxes and their associated surveillances were impacted by the performance deficiency. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green)because it:
: (1) did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components; and
: (2) did not involve an actual reduction in function of hydrogen igniters in the reactor containment. The finding had a cross-cutting aspect in the area of human performance associated with work management. Specifically, the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority, including the identification and management of risk commensurate with opening terminal box 392 during surveillance testing [H.5].  


The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the SSC and barrier performance attribute of the Barrier Integrity Cornerstone, and adversely affected the cornerstone objective to ensure the radiological barrier functionality of containment isolation. Specifically, with terminal box 392 open, its environmental qualification was temporarily invalidated, making the HPCI isolation instrumentation inoperable during surveillance testing. In addition, two other terminal boxes and their associated surveillances were impacted by the performance deficiency. Using Inspection Manual Chapter 0609, Appendix A, "The Significance Determination Process (SDP) for Findings At
=====Enforcement.=====
-Power," dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because it:  (1)did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components; and (2) did not involve an actual reduction in function of hydrogen igniters in the reactor containment. The finding had a cross
Technical Specification 5.4.1.a, requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A to Regulatory Guide 1.33, Quality Assurance Program Requirements, of February 1978. Section 1.f of Appendix A to Regulatory Guide 1.33 requires specific procedures for scheduling surveillance tests and calibration. The licensee established Station Procedure 0.26, Surveillance Program, Revision 68, to schedule and control surveillance testing. Section 5 of Station Procedure 0.26 states, the Shift Manager shall: be aware of any other systems affected by the test and how they are affected. Contrary to the above, on January 14, 2016, the licensee failed to ensure that the shift manager was aware of any other systems affected by the test and how they were affected during HPCI isolation surveillance testing. Specifically, the licensee failed to assess the operability of all affected containment isolation instrumentation when maintenance personnel opened TB 392 during surveillance testing and temporarily invalidated its environmental qualification. As immediate corrective actions, the licensee identified additional TBs impacted by the performance deficiency, and implemented Standing Order 2016-03, which directed operators to either establish compensatory measures or declare the affected equipment inoperable when environmentally qualified TB would be opened during testing. This violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy, because it was of very low safety significance (Green) and was entered into the licensees corrective action program as Condition Reports CR-CNS-2016-0320 and CR-CNS-2016-00476. (NCV 05000298/2016001-02, Failure to Assess Operability of Technical Specification System Functions during Surveillance Testing)
-cutting aspect in the area of human performance associated with work management. Specifically, the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority, including the identification and management of risk commensurate with opening terminal box 392 during surveillance testing [H.5].
Enforcement
. Technical Specification 5.4.1.a, requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A to Regulatory Guide 1.33, "Quality Assurance Program Requirements," of February 1978. Section 1.f of Appendix A to Regulatory Guide 1.33 requires specific procedures for scheduling surveillance tests and calibration. The licensee established Station Procedure 0.26, "Surveillance Program," Revision 68, to schedule and control surveillance testing. Section 5 of Station Procedure 0.26 states, the "Shift Manager shall:
be aware of any other systems affected by the test and how they are affected.Contrary to the above, on January 14, 2016, the licensee failed to ensure that the shift manager was aware of any other systems affected by the test and how they were affected during HPCI isolation surveillance testing.


Specifically, the licensee failed to assess the operability of all affected containment isolation instrumentation when maintenance personnel opened TB 392 during surveillance testing and temporarily invalidated its environmental qualification.
===Cornerstone: Emergency Preparedness===
{{a|1EP6}}


As immediate corrective actions, the licensee identified additional TBs impacted by the performance deficiency, and implemented Standing Order 2016-03, which directed operators to either establish compensatory measures or declare the affected equipment inoperable when environmentally qualified TB would be opened during testing.
This violation is being treated as a non
-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy, because it was of very low safety significance (Green) and was entered into the licensee's corrective action program as Condition Report s CR-CNS-2016-0320 and CR-CNS-2016-00476.  (NCV 05000298/2016001
-02, "Failure to Assess Operability of Technical Specification System Functions during Surveillance Testing")
===Cornerstone:===
Emergency Preparedness
{{a|1EP6}}
==1EP6 Drill Evaluation==
==1EP6 Drill Evaluation==
{{IP sample|IP=IP 71114.06}}
{{IP sample|IP=IP 71114.06}}
Line 406: Line 327:


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors observed an emergency preparedness drill on March 29, 2016, to verify the adequacy and capability of the licensee's assessment of drill performance. The inspectors reviewed the drill scenario, observed the drill from the Technical Support Center (TSC) and Simulator, and attended the post
The inspectors observed an emergency preparedness drill on March 29, 2016, to verify the adequacy and capability of the licensees assessment of drill performance. The inspectors reviewed the drill scenario, observed the drill from the Technical Support Center (TSC) and Simulator, and attended the post-drill critique. The inspectors verified that the licensees emergency classifications, off-site notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the licensee in the post-drill critique and entered into the corrective action program for resolution.
-drill critique. The inspectors verified that the licensee's emergency classifications, off
-site notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the licensee in the post-drill critique and entered into the corrective action program for resolution.


These activities constitute d completion of one emergency preparedness drill observation sample, as defined in Inspection Procedure 71114.06.
These activities constituted completion of one emergency preparedness drill observation sample, as defined in Inspection Procedure 71114.06.


====b. Findings====
====b. Findings====
Line 416: Line 335:


==RADIATION SAFETY==
==RADIATION SAFETY==
Cornerstones:
Cornerstones: Public Radiation Safety and Occupational Radiation Safety {{a|2RS2}}
Public Radiation Safety and Occupational Radiation Safety
 
{{a|2RS2}}
==2RS2 Occupational ALARA Planning and Controls==
==2RS2 Occupational ALARA Planning and Controls==
{{IP sample|IP=IP 71124.02}}
{{IP sample|IP=IP 71124.02}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors assessed licensee performance with respect to maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA). The inspectors performed this portion of the attachment as a post
The inspectors assessed licensee performance with respect to maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA). The inspectors performed this portion of the attachment as a post-outage review. During the inspection the inspectors interviewed licensee personnel, reviewed licensee documents, and evaluated licensee performance in the following areas:
-outage review. During the inspection the inspectors interviewed licensee personnel, reviewed licensee documents, and evaluated licensee performance in the following areas:
* Radiological work planning, including work activities of exposure significance, and radiological work planning ALARA evaluations, initial and revised exposure estimates, and exposure mitigation requirements. The inspectors also verified that the licensees planning identified appropriate dose reduction techniques, reviewed any inconsistencies between intended and actual work activity doses, and determined if post-job (work activity) reviews were conducted to identify lessons learned. Specific work plans reviewed included refuel floor activities for the refuel bridge upgrades and radwaste processing for High-Integrity Container (HIC) preparations for shipping.
Radiological work planning, including work activities of exposure significance,  
* Verification of dose estimates and exposure tracking systems including the basis for exposure estimates, and measures to track, trend, and if necessary reduce occupational doses for ongoing work activities. The inspectors evaluated the licensees method for adjusting exposure estimates and reviewed the licensees evaluations of inconsistent or incongruent results from the licensees intended radiological outcomes.
* Problem identification and resolution for ALARA planning and controls. The inspectors reviewed audits, self-assessments, work-in-progress and post-job ALARA reviews, and corrective action program documents to verify problems were being identified and properly addressed for resolution.


and radiological work planning ALARA evaluations, initial and revised exposure estimates, and exposure mitigation requirements.
These activities constituted completion of two of the five required samples of occupational ALARA planning and controls, as defined in Inspection Procedure 71124.02.


The inspectors also verified that the licensee's planning identified appropriate dose reduction techniques, reviewed any inconsiste ncies between intended and actual work activity doses, and determined if post
====b. Findings====
-job (work activity) reviews were conducted to identify lessons learned. Specific work plans reviewed included refuel floor activities for the refuel bridge upgrades and radwaste processing for High
No findings were identified. {{a|2RS4}}
-Integrity Container (HIC) preparations for shipping.


Verification of dose estimates and exposure tracking systems including the basis for exposure estimates, and measures to track, trend, and if necessary reduce occupational doses for ongoing work activities. The inspectors evaluated the licensee's method for adjusting exposure estimates and reviewed the licensee's evaluations of inconsistent or incongruent results from the licensee's intended radiological outcomes.
Problem identification and resolution for ALARA planning and controls. The inspectors reviewed audits, self
-assessments, work
-in-progress and post
-job ALARA reviews, and corrective action program documents to verify problems were being identified and properly addressed for resolution.
These activities constitute d completion of two of the five required samples of occupational ALARA planning and controls
, as defined in Inspection Procedure 71124.02.
====b. Findings====
No findings were identified.
{{a|2RS4}}
==2RS4 Occupational Dose Assessment==
==2RS4 Occupational Dose Assessment==
{{IP sample|IP=IP 71124.04}}
{{IP sample|IP=IP 71124.04}}


====a. Inspection Scope====
====a. Inspection Scope====
The inspectors evaluated the accuracy and operability of the licensee's personnel monitoring equipment, verified the accuracy and effectiveness of the licensee's methods for determining total effective dose equivalent, and verified that the licensee was appropriately monitoring occupational dose.
The inspectors evaluated the accuracy and operability of the licensees personnel monitoring equipment, verified the accuracy and effectiveness of the licensees methods for determining total effective dose equivalent, and verified that the licensee was appropriately monitoring occupational dose. The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance in the following areas:
 
* Source term characterization, including characterization of radiation types and energies, hard-to-detect isotopes, and scaling factors.
The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance in the following areas:
* External dosimetry, including National Voluntary Laboratory Accreditation Program (NVLAP) accreditation, storage, issue, use, and processing of active and passive dosimeters.
Source term characterization, including characterization of radiation types and energies, hard
* The technical competency and adequacy of the licensees internal dosimetry program.
-to-detect isotopes, and scaling factor s.
* Adequacy of the dosimetry program for special dosimetry situations, such as declared pregnant workers, multiple dosimetry placement, effective dose equivalent for external exposures (EDEX), shallow dose equivalent, neutron dose assessment, and dose records.
 
* Problem identification and resolution for occupational dose assessment, including audits, self-assessments, and corrective action documents.
External dosimetry
, including National Voluntary Laboratory Accreditation Program (NVLAP) accreditation, storage, issue, use, and processing of active and passive dosimeters
.
 
The technical competency and adequacy of the licensee's internal dosimetry program.
 
Adequacy of the dosimetry program for special dosimetry situations, such as declared pregnant workers, multiple dosimetry placement, effective dose equivalent for external exposures (EDEX), shallow dose equivalent, neutron dose assessment, and dose records.
 
Problem identification and resolution for occupational dose assessment, including audits, self
-assessments, and corrective action documents.


These activities constitute d completion of five occupational dose assessment inspection samples, as defined in Inspection Procedure 71124.04.
These activities constituted completion of five occupational dose assessment inspection samples, as defined in Inspection Procedure 71124.04.


====b. Findings====
====b. Findings====
Line 473: Line 368:


==OTHER ACTIVITIES==
==OTHER ACTIVITIES==
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security
{{a|4OA1}}
{{a|4OA1}}
==4OA1 Performance Indicator Verification==
==4OA1 Performance Indicator Verification==
{{IP sample|IP=IP 71151}}
{{IP sample|IP=IP 71151}}
===.1 Unplanned Scrams per 7000 Critical Hours (IE01)===
===.1 Unplanned Scrams per 7000 Critical Hours (IE01)===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed licensee event reports (LERs) for the period of January 1 through December 31, 2015, to determine the number of scrams that occurred. The inspectors compared the number of scrams reported in these LERs to the number reported for the performance indicator. Additionally, the inspectors sampled monthly operating logs to verify the number of critical hours during the period.
The inspectors reviewed licensee event reports (LERs) for the period of January 1 through December 31, 2015, to determine the number of scrams that occurred. The inspectors compared the number of scrams reported in these LERs to the number reported for the performance indicator. Additionally, the inspectors sampled monthly operating logs to verify the number of critical hours during the period. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the data reported.


The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the data reported.
These activities constituted verification of the unplanned scrams per 7000 critical hours performance indicator, as defined in Inspection Procedure 71151.
 
These activities constituted verification of the unplanned scrams per 7000 critical hours performance indicator
, as defined in Inspection Procedure 71151.


====b. Findings====
====b. Findings====
Line 491: Line 384:


===.2 Unplanned Power Changes per 7000 Critical Hours (IE03)===
===.2 Unplanned Power Changes per 7000 Critical Hours (IE03)===
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors reviewed operating logs, corrective action program records, and monthly operating reports for the period of January 1 through December 31, 2015, to determine the number of unplanned power changes that occurred. The inspectors compared the number of unplanned power changes documented to the number reported for the performance indicator. Additionally, the inspectors sampled monthly operating logs to verify the number of critical hours during the period. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, "Regulatory Assessment Performance Indicator Guideline," Revision 7, to determine the accuracy of the data reported.
The inspectors reviewed operating logs, corrective action program records, and monthly operating reports for the period of January 1 through December 31, 2015, to determine the number of unplanned power changes that occurred. The inspectors compared the number of unplanned power changes documented to the number reported for the performance indicator. Additionally, the inspectors sampled monthly operating logs to verify the number of critical hours during the period. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the data reported.


These activities constituted verification of the unplanned power changes per 7000 critical hours performance indicator, as defined in Inspection Procedure 71151.
These activities constituted verification of the unplanned power changes per 7000 critical hours performance indicator, as defined in Inspection Procedure 71151.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified. {{a|4OA2}}


{{a|4OA2}}
==4OA2 Problem Identification and Resolution==
==4OA2 Problem Identification and Resolution==
 
{{IP sample|IP=IP 71152}}
(71152)


===.1 Routine Review===
===.1 Routine Review===
====a. Inspection Scope====
====a. Inspection Scope====
Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensee's corrective action program and periodically attended the licensee's condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified.
Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.
 
The inspectors also reviewed the licensee's problem identification and resolution activities during the performance of the other inspection activities documented in this report.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


===.2 Annual Follow===
===.2 Annual Follow-up of Selected Issues===
 
-up of Selected Issues
 
====a. Inspection Scope====
====a. Inspection Scope====
The inspectors selected two issues for an in
The inspectors selected two issues for an in-depth follow-up:
-depth follow
* On January 6, 2016, the inspectors reviewed entries in the control room log from the previous night shift, which discussed the identification of leakage into the scram discharge volume (SDV). Operations personnel had isolated the SDV in advance of performing planned maintenance on the system, in order to quantify any potential leakage into the SDV, if it existed. During this activity, operators determined that there was no leakage into the North SDV, but the South SDV indicated leakage accumulating at a rate of 5.2 inches per hour. The inspectors noted that this was an indication of scram outlet valve leakage, and also observed that no condition report (CR) was written for the leakage that was discovered. In response to inspector questions, operations personnel took action to initiate a CR (CR-CNS-2016-00075) and assess operability. The inspectors noted that the site had failed to meet the requirements of Step 5.3.6.3 of Procedure 0-CNS-LI-102, Corrective Action Process, which required, in part, that individuals ensure the condition was promptly documented on a Condition Report, by no later than the end of their shift.
-up: On January 6, 2016, the inspectors reviewed entries in the control room log from the previous night shift, which discussed the identification of leakage into the scram discharge volume (SDV). Operations personnel had isolated the SDV in advance of performing planned maintenance on the system
, in order to quantify any potential leakage into the SDV, if it existed. During this activity, operators determined that there was no leakage into the North SDV, but the South SDV indicated leakage accumulating at a rate of 5.2 inches per hour. The inspectors noted that this was an indication of scram outlet valve leakage, and also observed that no condition report (CR) was written for the leakage that was discovered.


In response to inspector questions, operations personnel took action to initiate a CR (CR
In subsequent follow-up with the licensee, the inspectors learned that the CR had been considered a non-adverse condition, and as a result, CR generation had not been required. The CR had been classified as a D-trend non-adverse condition and closed. After further review, the inspectors determined that the condition met the licensee and NRC definition of a condition adverse to quality because the issue was a condition of an SSC, including failures and deficiencies, that could potentially render the SSC degraded or inoperable. Specifically, as discussed in GE SIL 173, a leaking scram [outlet] valve is of concern as the control rod drive (CRD) runs hot due to reactor water passing down through the drive and out the line to the scram discharge volume, and will continue to run hotter as the scram valve seat continues to erode. Eventually this could interfere with normal drive movement. In addition, the inspectors determined that scram outlet valve leakage into the SDV could result in high SDV water levels and undesirable scram signals if isolated, and could result in CRD drift if the leakage became excessive.
-CNS-2016-00075) and assess operability. The inspectors noted that the site had failed to meet the requirements of Step 5.3.6.3 of Procedure 0-CNS-LI-102, "Corrective Action Process," which required, in part, that individuals ensure the condition was promptly documented on a Condition Report, by no later than the end of their shift.


In subsequent follow
The inspectors determined that this issue represented a minor violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, which requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings of a type appropriate to the circumstances. Licensee procedure 0-CNS-LI-102, Corrective Action Process, an Appendix B quality related procedure, provides instructions for identifying and classifying conditions adverse to quality. Procedure 0-CNS-LI-102, Attachment 1, states in part, that adverse conditions are required to be corrected in the Corrective Action Program (CAP)and are subject to the rigor necessary to evaluate and thoroughly resolve important and significant issues. Contrary to the above, between January 6, 2016, and March 17, 2016, the licensee failed to assure that an adverse condition was corrected in the CAP and was subject to the rigor necessary to evaluate and thoroughly resolve important and significant issues.
-up with the licensee, the inspectors learned that the CR had been considered a non
-adverse condition, and as a result, CR generation had not been required.


The CR had been classified as a D
Specifically, the licensee initially failed to generate a condition report for indicated scram outlet valve leakage, and subsequently failed to classify the CR as a condition adverse to quality to ensure the deficiency would be resolved in the CAP. Instead, the CR was classified as D-Trend, which denotes a non-adverse condition that is handled outside of the CAP. The issue was minor in accordance with Inspection Manual Chapter 0612 Appendix B due to the minimal quantity of leakage identified and because other programmatic opportunities existed to identify the condition prior to significant plant impacts. Although this issue should be corrected, it constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section 2 of the Enforcement Policy. The issue was entered into the licensees CAP as CR-CNS-2016-01485. Licensee investigation revealed one CRD with slightly elevated temperatures, and the licensee generated a work order to repair the associated scram outlet valve.
-trend non
-adverse condition and closed. After further review, the inspectors determined that the condition met the licensee and NRC definition of a condition adverse to quality because the issue was a condition of an SSC, including failures and deficiencies, that could potentially render the SSC degraded or inoperable. Specifically, as discussed in GE SIL 173, "a leaking scram
[outlet] valve is of concern as the control rod drive (CRD) runs hot due to reactor water passing down through the drive and out the line to the scram discharge volume, and will continue to run hotter as the scram valve seat continues to erode. Eventually this could interfere with normal drive movement."  In addition, the inspectors determined that scram outlet valve leakage into the SDV could result in high SDV water levels and undesirable scram signals if isolated, and could result in CRD drift if the leakage


became excessive.
The inspectors assessed the licensees problem identification threshold and corrective actions to address the issue. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition.
* On January 11, 2016, the licensee identified that the Division 1 emergency diesel generator (EDG) was slow to start during a monthly surveillance test.


The inspectors determined that this issue represented a minor violation of 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and Drawings," which requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings of a type appropriate to the circumstances. Licensee procedure 0-CNS-LI-102, "Corrective Action Process
Specifically, the EDG achieved rated voltage and frequency in 14.2 seconds, which exceeded the surveillance requirement limit of 14 seconds. The delayed start was linked to a degraded shuttle valve in the non-safety portion of the air start system, which is normally bypassed during an emergency EDG start. The licensee determined that the apparent cause of the degradation was inadequate manufacturer controls of the component.
," an Appendix B quality related procedure, provides instructions for identifying and classifying conditions adverse to quality. Procedure 0-CNS-LI-102, Attachment 1, states in part, that "adverse conditions are required to be corrected in the Corrective Action Program (CAP) and are subject to the rigor necessary to evaluate and thoroughly resolve important and significant issues."  Contrary to the above, between January 6, 2016, and March 17, 2016, the licensee failed to assure that an adverse condition was corrected in the CAP and was subject to the rigor necessary to evaluate and thoroughly resolve important and significant issues
. Specifically, the licensee initially failed to generate a condition report for indicated scram outlet valve leakage, and subsequently failed to classify the CR as a condition adverse to quality to ensure the deficiency would be resolved in the CAP. Instead, the CR was classified as D
-Trend, which denotes a non
-adverse condition that is handled outside of the CAP. The issue was minor in accordance with Inspection Manual Chapter 0612 Appendix B due to the minimal quantity of leakage identified and because other programmatic opportunities existed to identify the condition prior to significant plant impacts. Although this issue should be corrected, it constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section 2 of the Enforcement Policy. The issue was entered into the licensee's CAP as CR-CNS-2016-01485. Licensee investigation revealed one CRD with slightly elevated temperatures, and the licensee generated a work order to repair the associated scram outlet valve.


The inspectors assessed the licensee's problem identification threshold and corrective actions to address the issue. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition
The inspectors assessed the licensees problem identification threshold, cause analyses, and extent of condition reviews. The inspectors verified that the licensee appropriately prioritized the corrective actions and that these actions were adequate to correct the condition.
.


On January 11, 2016, the licensee identified that the Division 1 emergency diesel generator (EDG) was slow to start during a monthly surveillance test. Specifically, the EDG achieved rated voltage and frequency in 14.2 seconds, which exceeded the surveillance requirement limit of 14 seconds. The delayed start was linked to a degraded shuttle valve in the non
These activities constituted completion of two annual follow-up samples as defined in Inspection Procedure 71152.
-safety portion of the air start system, which is normally bypassed during an emergency EDG start. The licensee determined that the apparent cause of the degradation was inadequate manufacturer controls of the component.
 
The inspectors assessed the licensee's problem identification threshold, cause analyses, and extent of condition reviews. The inspectors verified that the licensee appropriately prioritized the corrective actions and that these actions were adequate to correct the condition. These activities constitute d completion of two annual follow
-up samples as defined in Inspection Procedure 71152.


====b. Findings====
====b. Findings====
No findings were identified.
No findings were identified.


{{a|4OA5}}
{{a|4OA5}}
 
==4OA5 Other Activities==
==4OA5 Other Activities==
(Closed) Notice of Violation 05000298/2015007-04, Failure to Evaluate the Lack of Missile Protection on the Emergency Diesel Generator 1 and 2 Fuel Oil Storage Tank Vents, EA-15-089 During the Component Design Basis Inspection conducted on April 6 through May 8, 2015, a violation of NRC regulations was identified and documented in NRC Inspection Report 05000298/2015007 (ML15173A450). The NRC had determined that a cited violation was associated with the inspection. The violation was cited because Cooper Nuclear Station (CNS) failed to restore compliance with NRC requirements within a reasonable amount of time after a previous violation was identified in NRC Inspection Report 05000298/2010007 (ML103370640).


(Closed) Notice of Violation 05000298/2015007
In 2015, the team identified a Green, cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, which states, in part, Design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. Specifically, the licensee failed to verify the adequacy of design of the vents for the emergency diesel generator (EDG) 1 and 2 fuel oil storage tanks to withstand impact from a tornado driven missile hazard, or to evaluate for exemption from missile protection requirements using an approved methodology.
-04, Failure to Evaluate the Lack of Missile Protection on the Emergency Diesel Generator 1 and 2 Fuel Oil Storage Tank Vents, EA 089 During the Component Design Basis Inspection conducted on April 6 through May 8, 2015, a violation of NRC regulations was identified and documented in NRC Inspection Report 05000298/2015007 (ML15173A450). The NRC had determined that a cited violation was associated with th e inspection.


The violation was cited because Cooper Nuclear Station (CNS) failed to restore compliance with NRC requirements within a reasonable amount of time after a previous violation was identified in NRC Inspection Report 05000298/2010007 (ML103370640
The Notice of Violation (NOV) issued with the Inspection Report on June 22, 2015, required Cooper Nuclear Station to submit a written statement to the NRC within 30 days. The reply was required to contain the corrective steps taken to ensure full compliance was achieved. Cooper Nuclear Station submitted the response to the NRC on July 22, 2015 (ML15215A369). The corrective steps taken by the licensee included:
). In 2015, the team identified a Green, cited violation of 10 CFR Part 50, Appendix B, Criterion III, "Design Control," which states, in part, "Design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program."  Specifically, the licensee failed to verify the adequacy of design of the vents for the emergency diesel generator (EDG) 1 and 2 fuel oil storage tanks to withstand impact from a tornado driven missile hazard, or to evaluate for exemption from missile protection requirements using an approved methodology.
: (1) incorporating a compilation of CNS and industry documentation into an engineering report to substantiate the conclusions of the design basis documents that evaluated the EDG fuel oil storage tank vents ability to perform their design function following a design basis missile strike;
: (2) removing the cap on the storage tank fill opening and installing a screen to ensure operability per the associated work order;
: (3) reinforcing with engineers qualified to prepare or review calculations, the need to explicitly and literally state the technical issues when performing calculations;
: (4) incorporating lessons learned from the apparent cause evaluation as part of the Technical Rigor topic during engineering continuing training; and
: (5) revising NEDC 13-046, Revision 1, to directly address all four tornado impact scenarios as described in Section XII, 2.3.3.2 of the CNS Updated Safety Analysis Report.


The Notice of Violation (NOV) issued with the Inspection Report on June 22, 2015, required Cooper Nuclear Station to submit a written statement to the NRC within 30 days. The reply was required to contain the corrective steps taken to ensure full compliance was achieved. Cooper Nuclear Station submitted the response to the NRC on July 22, 2015 (ML15215A369). The corrective steps taken by the licensee included:
The NRC responded in a letter to Cooper Nuclear Stations response on August 11, 2015 (ML15224B562). The letter stated that the NRC would inform the licensee if further inspection was warranted. The inspector reviewed the licensees corrective actions associated with the violation. Specifically, the inspector reviewed Engineering Change EC-EE15-012, Diesel Generator Diesel Oil Tank Vents Tornado Missile Analysis, Revision 1, and Calculation NEDC 13-046, Diesel Generator Storage Vent Line Tornado Missile Durability, Revision 2. Based on this review, the inspector concluded that the licensee had performed adequate corrective actions to restore compliance, address extent of condition, and prevent recurrence. No additional deficiencies were identified during the review of this Notice of Violation.
(1) incorporating a compilation of CNS and industry documentation into an engineering report to substantiate the conclusions of the design basis documents that evaluated the EDG fuel oil storage tank vents' ability to perform their design function following a design basis missile strike; (2) removing the cap on the storage tank fill opening and installing a screen to ensure operability per the associated work order; (3) reinforcing with engineers qualified to prepare or review calculations, the need to explicitly and literally state the technical issues when performing calculations; (4)incorporating lessons learned from the apparent cause evaluation as part of the Technical Rigor topic during engineering continuing training; and (5) revising NEDC 13-046, Revision 1, to directly address all four tornado impact scenarios as described in Section XII, 2.3.3.2 of the CNS Updated Safety Analysis Report. The NRC responded in a letter to Cooper Nuclear Station's response on August 11, 2015 (ML15224B562). The letter stated that the NRC would inform the licensee if further inspection was warranted. The inspector reviewed the licensee's corrective actions associated with the violation. Specifically, the inspector reviewed Engineering Change EC-EE15-012, "Diesel Generator Diesel Oil Tank Vents Torn ado Missile Analysis," Revision 1, and Calculation NEDC 13-046, "Diesel Generator Storage Vent Line Tornado Missile Durability," Revision 2. Based on this review, the inspector concluded that the licensee had performed adequate corrective actions to restore compliance, address extent of condition, and prevent recurrence. No additional deficiencies were identified during the review of this Notice of Violation.
 
This review closes NOV 05000298/2015007-04, Failure to Evaluate the Lack of Missile Protection on the Emergency Diesel Generator 1 and 2 Fuel Oil Storage Tank Vents, EA-15-089.


This review closes NOV 05000298/2015007
-04, "Failure to Evaluate the Lack of Missile Protection on the Emergency Diesel Generator 1 and 2 Fuel Oil Storage Tank Vents,
" EA-15-089.
{{a|4OA6}}
{{a|4OA6}}
==4OA6 Meetings, Including Exit==
==4OA6 Meetings, Including Exit==
===Exit Meeting Summary===
===Exit Meeting Summary===
On March 24, 2016, the inspectors presented the results of the diesel fuel oil tank Notice of Violation closure review to Mr. D. Buman, Director of Engineering, and other members of the licensee staff via telephone. The licensee acknowledged the inspection results. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On March 24, 2016, the inspectors presented the results of the diesel fuel oil tank Notice of Violation closure review to Mr. D. Buman, Director of Engineering, and other members of the licensee staff via telephone. The licensee acknowledged the inspection results. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


On March 24, 2016, the inspectors presented the radiation safety inspection results to Mr. K. Higginbotham, General Manager, Plant Operations, and other members of the licensee staff. The licensee acknowledged the inspection results
On March 24, 2016, the inspectors presented the radiation safety inspection results to Mr. K. Higginbotham, General Manager, Plant Operations, and other members of the licensee staff. The licensee acknowledged the inspection results. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.


On April 8, 2016, the inspectors presented the inspection results to Mr. O. Limpias, Vice President and Chief Nuclear Officer, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
On April 8, 2016, the inspectors presented the inspection results to Mr. O. Limpias, Vice President and Chief Nuclear Officer, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.
Line 587: Line 456:


==KEY POINTS OF CONTACT==
==KEY POINTS OF CONTACT==
===Licensee Personnel===
===Licensee Personnel===
: [[contact::T. Barker]], Manager, Engineering Program and Components
: [[contact::T. Barker]], Manager, Engineering Program and Components  
: [[contact::J. Bebb]], Staff Health Physicist, Radiation Protection
: [[contact::J. Bebb]], Staff Health Physicist, Radiation Protection  
: [[contact::D. Buman]], Director, Engineering
: [[contact::D. Buman]], Director, Engineering  
: [[contact::B. Chapin]], Manager, Maintenance
: [[contact::B. Chapin]], Manager, Maintenance  
: [[contact::T. Chard]], Manager, Quality Assurance
: [[contact::T. Chard]], Manager, Quality Assurance  
: [[contact::L. Dewhirst]], Manager, Corrective Action and Assessment
: [[contact::L. Dewhirst]], Manager, Corrective Action and Assessment  
: [[contact::K. Dia]], Manager, System Engineering
: [[contact::K. Dia]], Manager, System Engineering  
: [[contact::J. Dixon]], Supervisor, Radiation Protection
: [[contact::J. Dixon]], Supervisor, Radiation Protection  
: [[contact::R. Estrada]], Manager, Design Engineering
: [[contact::R. Estrada]], Manager, Design Engineering  
: [[contact::J. Flaherty]], Senior Staff Engineer, Licensing
: [[contact::J. Flaherty]], Senior Staff Engineer, Licensing  
: [[contact::T. Forland]], Engineer, Licensing
: [[contact::T. Forland]], Engineer, Licensing  
: [[contact::D. Goodman]], Manager, Operations  
: [[contact::D. Goodman]], Manager, Operations  
: [[contact::K. Higginbotham]], General Manager, Plant Operations
: [[contact::K. Higginbotham]], General Manager, Plant Operations  
: [[contact::D. Kimball]], Director, Nuclear
: [[contact::D. Kimball]], Director, Nuclear Oversight  
Oversight
: [[contact::O. Limpias]], Vice President, Chief Nuclear Officer  
: [[contact::O. Limpias]], Vice President, Chief Nuclear Officer
: [[contact::J. Olberding]], Licensing Engineer, Regulatory Affairs  
: [[contact::J. Olberding]], Licensing Engineer, Regulatory Affairs
: [[contact::R. Penfield]], Director, Nuclear Safety Assurance  
: [[contact::R. Penfield]], Director, Nuclear Safety Assurance
: [[contact::J. Shaw]], Manager, Licensing  
: [[contact::J. Shaw]], Manager, Licensing  
: [[contact::J. Stough]], Manager, Emergency Preparedness
: [[contact::J. Stough]], Manager, Emergency Preparedness  
: [[contact::C. Sunderman]], Manager,
: [[contact::C. Sunderman]], Manager, Radiation Protection  
Radiation Protection


==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
==LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED==
===Opened and Closed===
: 05000298/2016001-01 NCV Failure to Follow ASME Code Requirements when taking Corrective Actions for a Pump in the Required Action Range (Section 1R22)
: 05000298/2016001-02 NCV Failure to Assess Operability of Technical Specification System Functions during Surveillance Testing (Section 1R22)


===Opened and Closed===
: 05000298/2016001-01 NCV Failure to Follow ASME Code Requirements when taking Corrective Actions for a Pump in the Required Action Range
(Section 1R22)
: 05000298/2016001
-02 NCV Failure to Assess Operability of Technical Specification System Functions during Surveillance Testing (Section
1R22) 
===Closed===
===Closed===
: 05000298/2015007
: 05000298/2015007-04 VIO Failure to Evaluate the Lack of Missile Protection on the Emergency Diesel Generator 1 and 2 Fuel Oil Storage Tank Vents (Section 4OA5)  
-04 VIO Failure to Evaluate the Lack of Missile Protection on the Emergency Diesel Generator 1 and 2 Fuel Oil Storage Tank Vents (Section 4OA5)  


==LIST OF DOCUMENTS REVIEWED==
==LIST OF DOCUMENTS REVIEWED==
Section 1R04
:
: Equipment Alignment
===Miscellaneous Documents===
: Number Title Revision E501 Burns and Roe, SW
-MOV-36 SW Loop Cross Tie Header Isolation Valve, Sheet 11A
: N01 E501 Burns and Roe, SW
-MOV-37 SW Pumps Cross Tie Header Isolation Valve, Sheet 11B
: CNS-EQ-122 Cooper Nuclear Station EQ Configuration Terminal Boxes and Equipment Enclosures, Sheet 1
: CNS-EQ-122 Cooper Nuclear Station EQ Configuration Terminal Boxes and Equipment Enclosures, Sheet 2
: 00-111 NEDC, CNS Auxiliary Power System AC Loads
: 11-140 NEDC, Review of ZNE Calculation 11
-198, Revision 1, Cooper Nuclear Station Service Water System Analysis
: 12-019 NEDC, Service Water Post
-LOCA Flow Test Revised Acceptance Criteria
: 12-020 Engineering Evaluation, Service Water Post
-LOCA Flow Verification Test Revised Acceptance Criteria
: 87-0053 License Change Request
: 90-004 Design Change, Automatic Isolation of SW
-MOV-37MV on Low Service Water Pressure
: 94-021 NEDC, REC
-HX-A &
: REC-HX-B Maximum Allowable Accident Case Fouling
: 2007 Burns and Roe, Cooper Nuclear Station Flow Diagram Turbine Building Closed Cooling Water System
: 2031 Burns and Roe, Cooper Nuclear Station Flow Diagram Reactor Building
- Closed Cooling Water System, Sheet
: N65 2031 Burns and Roe, Cooper Nuclear Station Flow Diagram Reactor Building
- Closed Cooling Water System, Sheet
: 33 791E271 Cooper Nuclear Station Elementary Diagram HPCI System, Sheet 3 N23 791E271 Cooper Nuclear Station Elementary Diagram HPCI System, Sheet 4 N24 791E271 Cooper Nuclear Station Elementary Diagram HPCI System, Sheet 6 20
===Procedures===
: Number Title Revision 2.2A.REC.DIV
: Reactor Equipment Cooling Water System Component Checklist (DIV 1) 0 2.2A.REC.DIV 3
: Reactor Equipment Cooling Water System Common Divisional Component Checklist
: 2.2B.REC.DIV 1
: Reactor Equipment Cooling Water System Instrument Valve Checklist (DIV
: 1) 0 2.2.54A MPF Air System Component Checklist
: 2.2.65.1 REC Operations
: 2.2.69.3 RHR Suppression Pool Cooling and Containment Spray
: 2.2.70 RHR Service Water Booster Pump System
: 2.3_RHR-GLND-1 RHR Gland Water Supply
- Annunciator Panel 1A
: 2.3_RHR-GLND-1 RHR Gland Water Supply
- Annunciator Panel 1B
: 2.3_9-3-1 Panel 9-3 - Annunciator 9
-3-1 34 2.3_9-3-3 Panel 9-3 - Annunciator 9
-3-3 19 3.4.7 Design Calculations
: 3.4.8 Design Verification
: 5.3EMPWR Emergency Power During Modes 1, 2, or 3
: 6.SWBP.201
: SW-MO-89A/B Full Stroke Operability (IST)
: 6.1DG.302
: Undervoltage Logic Functional, Load Shedding, and Sequential Loading Test (DIV
: 1) 83
===Condition Reports===
(CRs)
: CR-CNS-2015-06035
: CR-CNS-2015-06754
: CR-CNS-2016-00045
: CR-CNS-2016-00091
: CR-CNS-2016-00238
: CR-CNS-2016-00449
: CR-CNS-2016-00458
: CR-CNS-2016-00460
: CR-CNS-2016-00469
: CR-CNS-2016-01117
: CR-CNS-2016-01129
===Work Orders===
: 5064786     
: Section 1R05
:
: Fire Protection
===Miscellaneous Documents===
: Number Title Revision 09-035 Engineering Evaluation, Evaluation of Fire Doors
: 11-088 Fire Safety Analysis for Fire Area CB
-D EPM Report R1906-008-CBD 3 11-090 NEDC
===Procedures===
: Number Title Revision
: CNS-FP-243 Reactor Feed Pump Area
: 0-Barrier Barrier Control Process
: 0-Barrier-Control Control Building
: 0-Barrier-Misc Miscellaneous Buildings
: 0-CNS-WM-104A On-Line Fire Risk Management Actions
: 0.7.1 Control of Combustibles
: 0.23 CNS Fire Protection Plan
: 6.FP.314 Panel 9-32 and 9-33 Incipient Smoke Detector Testing
===Condition Reports===
(CRs)
: CR-CNS-2013-08029
: CR-CNS-2015-00777
: CR-CNS-2015-00810
: CR-CNS-2015-07704
: Section 1R06
:
: Flood Protection Measures Miscellaneous Documents Number Title Revision 02-059 Engineering Evaluation, Maintaining Acceptable Water Level in SE Quad Following a DBA LOCA
: 09-102 NEDC, Internal Flooding
- HELB, MELB, and Feedwater Line Break
: 1, 1C4, 1C5
: 13-30 Engineering Evaluation, Internal Flooding
- HELB, MELB, and Feedwater Line Break
: 0, 1, 2, 3
: 93-128 NEDC, Flooding Interaction Between Torus Area and Quads
: 98-038 NEDC, Post LOCA Leakage in Rx Bldg Quad Sumps A
-E 3
===Miscellaneous Documents===
: Number Title Revision 2004 Burns and Roe
, Cooper Nuclear Station Flow Diagram Condensate and Feedwater Systems, Sheet 2
: N50 2004 Burns and Roe
, Cooper Nuclear Station Flow Diagram Condensate and Feedwater Sytems, Sheet 3
: 2013-016 USAR Change Request
: 2038 Burns and Roe
, Cooper Nuclear Station Flow Diagram Reactor Building Floor and Roof Drain Systems, Sheet 1
: N54
===Procedures===
: Number Title Revision 0.19 Equipment Record and Functional Location File Program
: 2.3_A-4 Panel A - Annunciator A
-4 44 2.3_B-3 Panel B- Annunciator B
-3 36 2.3_S-1 Panel S - Annunciator S
-1 24 2.4TEC TEC Abnormal
: 3-EN-DC-167 Classification of Structures, Systems, and Components
: 4C1 3.12.3 Environmental Qualification Design Input File Control
: 3.12.7 Control of Master Equipment List (MEL)
: 5.1Break Pipe Break Outside Secondary Containment
: 5.2Air Loss of Instrument Air
: 5.2REC Loss of REC
: 5.2SW Service Water Casualties
: 15.Sump.101
: Sump Pump Operability Test
===Condition Reports===
(CRs)
: CR-CNS-2012-09508
: CR-CNS-2015-02409
: CR-CNS-2015-02440 CR-CNS-2015-02441
==Section 1R11: Licensed Operator Requalification Program==
and Licensed Operator Performance
===Miscellaneous Documents===
: Number Title Date SKL0525287
: Exam Scenario 87
: January 21,
: 2016
===Procedures===
: Number Title Revision 2.2.65.1 REC Operations
: 6.MS.201 Main Steam Isolation Valve Operability Test (IST)
: 6.MS.301 Main Steam Isolation Valve Limit Switch Channel Calibration
===Condition Reports===
(CRs)
: CR-CNS-2016-00820
: Section 1R12
:
: Maintenance Effectiveness
===Miscellaneous Documents===
: Number Title Revision/Date
: Maintenance Rule Program Monthly Status Report January 15,
: 2016
: Maintenance Rule Program Monthly Status Report February 4,
: 2016
: Maintenance Rule Program Monthly Status Report March 3,
: 2016
: Reactor Recirc System Health Report January 2016
: RR-F01 Maintenance Rule Function Basis for RR
-F01 - Recirc Flow
: RRFC-F01 Maintenance Rule Function Basis for RRFC
-F01 - Recirc Speed 2
: RRMG-F01 Maintenance Rule Function Basis for RRMG
-F01 - Recirc MG Set Power
: RR-SD1 Maintenance Rule Function Basis for RR
-SD1 - Recirc During Shutdown Operations
===Procedures===
: Number Title Revision 2.1.10 Station Power Changes
: 109 3-EN-DC-205 Maintenance Rule Monitoring
: 5C0 5.8.19 Reference Leg Injection
: 6.1CS.102
: Reference Leg Injection Flow Verification and IST Check Valve Testing (Div 1)
===Procedures===
: Number Title Revision 6.1RR.302
: Reactor Recirculation Flow Unit Channel Calibration
: 6.2CS.102
: Reference Leg Injection Flow Verification and IST Check Valve Testing (Div 2)
===Condition Reports===
(CRs)
: CR-CNS-2015-02053
: CR-CNS-2015-05820
: CR-CNS-2016-00436
===Work Orders===
: 5054097
: 5062934
: 5062935
: 5071062
: Section 1R13
:
: Maintenance Risk Assessments and Emergent Work Control
===Miscellaneous Documents===
: Number Title Revision/Date
: CNS Station Log Entries for EDG2 Maintenance Window March 21
- March 24,
: 2016 PMIS MUX 0
: Computer P
oint Description January 27,
: 2016 PMIS MUX 9
: Computer Point Description January 27,
: 2016 2006 Burns and Roe, Cooper Nuclear Station Flow Control Building Service Water System, Sheet 4
: 2077 Burns and Roe, Flow Diagram
- Diesel Gen Bldg Service Water, Starting Air, Fuel Oil, Sump System and Roof Drains
: N78
===Procedures===
: Number Title Revision 0-CNS-WM-104 On-Line Schedule Risk Assessment
: 0-CNS-WM-104A On-Line Fire Risk Management Actions
: 0-PROTECT-EQP Protected Equipment Program
: 0.23 CNS Fire Protection Plan
: 2.1.10 Station Power Changes
: 110 2.2.20.1 Diesel Generator Operations
===Procedures===
: Number Title Revision 2.2.20.2 Operation of Diesel Generators from Diesel Generator Rooms 62 2.2.67 Reactor Core Isolation Cooling System
: 2.4COMP Computer Malfunction
: 2.6.3PMIS
: PMIS Computer System Operation and Outage Recovery
: 5.3EMPWR Emergency Power During Modes 1, 2, or 3
: 5.3SBO Station Blackout
: 7.0.1.7 Troubleshooting Plant Equipment
===Condition Reports===
(CRs)
: CR-CNS-2015-05822
: CR-CNS-2015-06175
: CR-CNS-2015-06608
: CR-CNS-2016-00013
: CR-CNS-2016-00141
: CR-CNS-2016-00167
: CR-CNS-2016-00401
: CR-CNS-2016-00478
: CR-CNS-2016-00479
: CR-CNS-2016-01334
===Work Orders===
: 4880369
: 5000241
: 5012617
: 5012812
: 5013072
: 5039798
: 5039799
: 5039865
: 5039883
: 5039914
: 5039939
: 5040167
: 5040181
: 5040240
: 5040256
: 5040267
: 5040563
: 5044341
: 5060554
: 5060555
: 5060556
: 5067965
: 5069986
: 5075110
: 5084777
: 5091681
: 5097718
: 5098563
: 5099449
: 5106337
: 5110836
: Section 1R15
:
: Operability Determinations and Functionality Assessments
===Miscellaneous Documents===
: Number Title Revision/Date
: IST Basis Document
: 03-001 NEDC, Service Water Pump Barge Impact Load Analysis
: 11-140 NEDC, Review of ZNE Calculation 11
-198, Revision 1, Cooper Nuclear Station Service Water System Analysis
: 12-019 NEDC, Service Water Post
-LOCA Flow Test Revised Acceptance Criteria
===Miscellaneous Documents===
: Number Title Revision/Date 12-028 NEDC, Sulzer Seismic Qualification Analysis for
: SW-P-CE12.5.192
: 1
: DCD-39 ISI Boundary Basis
- ASME Section XI Classification Document April 6, 2011
: ESD95081 CNS IST Issue Resolution February 20,
: 1995 2039 Flow Diagram, Control Rod Drive Hydraulic System
===Procedures===
: Number Title Revision 0.26 Surveillance Program 69 0.5OPS Operations Review of Condition Reports/Operability Determination
: 2.0.12 Operator Challenges
: 2.1.5 Reactor Scram
: 2.2.8 Control Rod Drive Hydraulic System
: 2.2.8A Control Rod Drive Hydraulic System Component Checklist
: 2.3_RHR-GLND-1 RHR Gland Water Supply
- Annunciator Panel 1A
: 2.3_RHR-GLND-2 RHR Gland Water Supply
- Annunciator Panel 1B
: 2.3_9-3-1 Panel 9-3 - Annunciator 9
-3-1 34 2.3_9-3-3 Panel 9-3 - Annunciator 9
-3-3 19 3.9 ASME OM Code Testing of Pumps and Valves 28 6.EE.607 125V Station Battery Modified Performance Discharge Test
: 21 6.EE.611 125V/250V Battery Cell and Rack Examination
: 6.MISC.502
: ASME Class 1 System Leakage Test
: 6.SW.102 Service Water System Post
-LOCA Flow Verification
: 6.1REC.101
: REC Surveillance Operation (IST)(DIV
: 1) 16 15.CRD.501
: CRD Hydraulic Control Unit Scram Discharge Valve Leakage Check
===Condition Reports===
(CRs)
: CR-CNS-2014-03251
: CR-CNS-2014-03489
: CR-CNS-2015-02053
: CR-CNS-2015-03158
: CR-CNS-2015-03538
: CR-CNS-2015-06035
: CR-CNS-2015-06703
: CR-CNS-2015-07228
: CR-CNS-2016-00045
: CR-CNS-2016-00057
: CR-CNS-2016-00075
: CR-CNS-2016-00091
: CR-CNS-2016-00201
: CR-CNS-2016-00784
: CR-CNS-2016-00920
: CR-CNS-2016-01448
: Section 1R18
:
: Plant Modifications
===Miscellaneous Documents===
: Number Title Revision
: 4899459 Engineering Change, 1200A, 4160V Vacuum Bottle Circuit Breaker Replacement
: 4899506 Engineering Change, 1200A, 4160V Vacuum Bottle Circuit Breaker Replacement EE
-CB-4160G (RSWP1B)
: 6024460 Change Evaluation Document, 4kV Auxiliary Switch Removal 0
===Condition Reports===
(CRs)
: CR-CNS-2016-00443
: CR-CNS-2016-00456
: Section 1R19
:
: Post-Maintenance Testing
===Procedures===
: Number Title Revision
: CNS-EQ-129 EQ Configuration Detail Limitorque
- Valve Actuator, Sheet 1
: 6.SWBP.201
: SW-MO-89A/B Full Stroke Operability
: 6.1DG.101
: Diesel Generator 31 Day Operability Test (IST)(DIV1)
: 6.1PC.203
: Suppression Chamber Reactor Building Vacuum Breaker Functional Test (DIV 1)
: 6.2PC.203
: Suppression Chamber Reactor Building Vacuum Breaker Functional Test (DIV 2)
: 6.2SWBP.101
: RHR Service Water Booster Pump Flow Test and Valve Operability Test (DIV 2)
: 7.0.5 CNS Post-Maintenance Testing
: 7.5.8 Limitorque Mechanical/Electrical Examination
: 7.5.12
: SMB-0 Through SMB
-4 MOV Refurbishment
===Condition Reports===
(CRs)
: CR-CNS-2013-00320
: CR-CNS-2015-02678
: CR-CNS-2016-00416
: CR-CNS-2016-00418
: CR-CNS-2016-00420
: CR-CNS-2016-00426
: CR-CNS-2016-00447
: CR-CNS-2016-00472
: CR-CNS-2016-00562
: CR-CNS-2016-00633
===Work Orders===
: 5013072
: 5016337
: 5039864
: 5039865
: 5040267
: 5040276
: 5040268
: 5040345
: 5040633
: 5040682
: 5054772
: 5077920
: 5082545
: Section 1R22
:
: Surveillance Testing
===Miscellaneous Documents===
: Number Title Revision/Date Station Log Entries for REC A IST
: February 12,
: 2016 3-EN-DC-304 MOV Thrust/TorqueSetpoint Calculations
: 1C0 11-140 NEDC, Post
-LOCA Service Water Flow
: 12-019 NEDC, Service Water Post
-LOCA Flow Test Revised Acceptance Criteria
: 12-020 Engineering Evaluation, Service Water Post
-LOCA Flow Verification Test Revised Acceptance Criteria
: 16-632 ASME Code Inquiry March 23,
: 2016 91-245 NEDC, Review of MPR's System Level Design Basis Review for Service Water System MOV's
: 95-003 NEDC, Determination of Allowable Operating Parameters for CNS MOV Program MOVs
: 2044 Flow Diagram
- High Pressure Coolant Injection and Reactor Feed Systems
: 11218203 ECR,
: REC-P-A Differential Pressure High and 1 GE SIL 336
: Surveillance Testing Recommendations for HPCI and RCIC Systems 1
: RP-08 Relief Request:
: Comprehensive Pump Test Upper Limit
===Procedures===
: Number Title Revision 0.26 Surveillance Program
: 68, 69 0.40.2 Control and Maintenance of CNS Surveillance Maintenance Plans/Task Lists
: 3.33 Motor Operated Valve Program
: 3.9 ASME OM Code Testing of Pumps and Valves 28 6.HPCI.103
: HPCI IST and 92 Day Test Mode Surveillance Operation
: 6.HPCI.301
: HPCI Steam Line Space Temperature Switch Functional Test
: 9 6.PCIS.601
: Steam Line Break Detection Temperature Switch Calibration Test (Bath)
: 6.SW.102 Service Water System Post
-LOCA Flow Verification
: 6.SW.202 Service Water Power Operated Valve Operability Test
: 6.1DG.101
: Diesel Generator 31 Day Operability Test (DIV
: 1) 82 6.1HPCI.701
: HPCI Steam Line High Flow Channel Funtional Test (DIV
: 1) 6 6.1HPCI.702
: HPCI Steam Line Low Pressure Channel Functional Test (DIV 1) 5 6.1REC.101
: REC Surveillance Operation (IST)(DIV
: 1) 16 6.2HPCI.702
: HPCI Steam Line Low Pressure Channel Functional Test (DIV 2) 5
===Condition Reports===
(CRs)
: CR-CNS-2016-00141
: CR-CNS-2016-00167
: CR-CNS-2016-00201
: CR-CNS-2016-00218
: CR-CNS-2016-00230
: CR-CNS-2016-00320
: CR-CNS-2016-00321
: CR-CNS-2016-00322
: CR-CNS-2016-00323
: CR-CNS-2016-00784
: CR-CNS-2016-00920
: Section 1EP6
:
: Drill Evaluation
===Miscellaneous Documents===
: Title Date
: EP Drill Scenario Overview
- 2016 Dress Rehearsal March 29, 2016
===Procedures===
: Number Title Revision 5.7.6 Emergency Notification
===Condition Reports===
(CRs)
: CR-CNS-2016-01722
: CR-CNS-2016-01723
: CR-CNS-2016-01727
: CR-CNS-2016-01730
: CR-CNS-2016-01731
: CR-CNS-2016-01737
: CR-CNS-2016-01738
: CR-CNS-2016-01738 CR-CNS-2016-01754
==Section 2RS2: Occupational==
: ALARA Planning and Controls Audits and Self
-Assessments Number Title Date
: LO-2014-180-004 Pre-NRC Inspection Assessment March 2015
: LO-2015-094-001 Maintenance Department 2015 Snap Shot Assessment December
: 2015
: LO-2015-201-003 Pre-NRC Inspection Assessment January 2016
===Miscellaneous Documents===
: Title Date
: 2015 Cooper Nuclear Station ALARA Program March 2016
: Cooper Daily Dose Projections March 21,
: 2016
: Cooper Nuclear Station 5
-Year CRE Reduction Plan; 2016
-2020 March 2016
: Selected Station ALARA Committee Meeting Minutes;
: 2015/2016
===Procedures===
: Number Title Revision 9.ALARA.4
: Radiation Work Permits
: 9.EN-RP-100 Radiation Worker Expectations
: 9.EN-RP-102 Radiological Control
: 9.EN-RP-110 ALARA Program
: 9.EN-RP-110-105 ALARA Planning and Controls
: 9.RADOP.1
: Radiation Protection at CNS
: Radiation Work Permits Number Title Revision 2016-004 All RCA Buildings General Entry
- All Crafts 00 2016-014 Refuel Floor Activities (Refuel Bridge Upgrade)
: 2016-102 HIC Preps / Shipments
===Condition Reports===
(CRs)
: CR-CNS-2015-02757
: CR-CNS-2015-04633
: CR-CNS-2015-04807
: CR-CNS-2015-04833
: CR-CNS-2015-05008
: CR-CNS-2015-05550
: CR-CNS-2015-05556
: CR-CNS-2015-05815
: CR-CNS-2015-05938
: CR-CNS-2015-06579
: CR-CNS-2015-07167
: CR-CNS-2016-00497
: CR-CNS-2016-00597 CR-CNS-2015-01109


==Section 2RS4: Occupational Dose Assessment==
: Audits and Self Assessments Number Title Date
: Radiation Protection Program Annual Report
: 2014 14-04 QA Audit of Radiological Controls September 9,
: 2014
: LO-2015-201-003 Focused Self
-Assessment:
: ALARA Planning and Controls and Occupational Dose Assessment January 15,
: 2016
===Miscellaneous Documents===
: Title Date
: 100555-0 National Voluntary Laboratory Accreditation Program (NVLAP) Certificate for Mirion Technologies June 11,
: 2015
: 2014 DAW Part 61 Analysis February 17,
: 2015
: Airborne Radioactivity Scaling Factor for Hard to Identify Nuclides (White Paper)
: June 9, 2013
: Internal Dose Assessment Prospectus
: 2015
: Internal Dose Assessment Prospectus
: 2016
===Procedures===
: Number Title Revision 9.ALARA.1
: Personnel Dosimetry and Occupational Radiation Exposure Program 44 9.ALARA.13
: Radiation Worker and Tour Group Dosimetry Management
: 9.EN-RP-102 Radiological Control
: 9.EN-RP-104 Personnel Contamination
: 9.EN-RP-110-05 ALARA Planning and Controls
: 9.EN-RP-122
: Alpha Monitoring
: 9.EN-RP-203 Dose Assessment
: 9.EN-RP-205 Prenatal Monitoring
: 9.EN-RP-206 Dosimeter of Legal Record Quality Assurance
: 9.EN-RP-208
: Whole Body Counting and In-Vitro Bioassay
: 9.EN-RP-210
: Area Radiation Monitoring
: 9.EN-RP-311 Electronic Alarming Dosimeters
: 9.RADOP.1
: Radiation Protection at CNS
: 9.RADOP.2
: Radiation Safety Standards and Limits
: 9.RADOP.5
: Airborne Radioactivity Sampling
===Condition Reports===
(CRs)
: CR-CNS-2014-00522
: CR-CNS-2014-00962
: CR-CNS-2014-01617
: CR-CNS-2014-02231
: CR-CNS-2014-03991
: CR-CNS-2014-05017
: CR-CNS-2014-05607
: CR-CNS-2014-05644
: CR-CNS-2014-05948
: CR-CNS-2014-06205
: CR-CNS-2014-06269
: CR-CNS-2014-06636
: CR-CNS-2014-06726
: CR-CNS-2014-06812
: CR-CNS-2014-07414
: CR-CNS-2015-00183
: CR-CNS-2015-01372
: CR-CNS-2015-01840
: CR-CNS-2015-04491
: CR-CNS-2016-00698
: Section 4OA1
:
: Performance Indicator Verification
===Procedures===
: Number Title Revision 0-EN-LI-114 Performance Indicator Process
: 5C2 
: Section 4OA2
:
: Problem Identification and Resolution
===Miscellaneous Documents===
: Number Title Revision/Date
: Failure Modes and Effects Analysis
- DG1 Slow Start
: IST Basis Document
: DCD-39 ISI Boundary Basis
- ASME Section XI Classification Document April 6, 2011
: ESD95081 CNS IST Issue Resolution February 20,
: 1995 ENDC 11209442
: DG1 Slow Start Time (CR
-CNS-2016-00141) January 12,
: 2016 GE SIL 173
: Control Rod Drive High Operating Temperature May 28, 1976
: 117.10-IC-09 EDG 1 Composite Control Air Schematic
: 2010 Burns and Roe, Flow Diagram
- Instrument Air Control and Turbine Building, Sheet
: A9 2039 Flow Diagram, Control Rod Drive Hydraulic System
: 2077 Burns and Roe, Flow Diagram
- Diesel Gen Bldg Service Water, Starting Air, Fuel Oil, Sump System and Roof Drains
: N78 45001 84705
: Purchase Order
- Valve PC8
: January 12,
: 2016
===Procedures===
: Number Title Revision 0-CNS-LI-102 Corrective Action Process
: 2.2.8 Control Rod Drive Hydraulic System
: 53, 91 2.2.8A Control Rod Drive Hydraulic System Component Checklist
: 2.2.20.2 Operation of Diesel Generators from Diesel Generator Rooms 62 6.MISC.502
: ASME Class 1 System Leakage Test
: 15.CRD.501
: CRD Hydraulic Control Unit Scram Discharge Valve Leakage Check
===Condition Reports===
(CRs)
: CR-CNS-2015-06608
: CR-CNS-2015-06927
: CR-CNS-2016-00075
: CR-CNS-2016-00141
: CR-CNS-2016-00167
: CR-CNS-2016-00194
: CR-CNS-2016-00403
: CR-CNS-2016-01301
: CR-CNS-2016-01485
: CR-CNS-2016-01523
: CR-CNS-2016-01755
===Work Orders===
: 22746
: 5028371
: 5044378
: 5115933 112094402
: Section 4OA5
:
: Other Activities
===Miscellaneous Documents===
: Number Title Revision
: EC-EE15-012 Diesel Generator Diesel Oil Tank Vent Tornado Missile Analysis 1 NEDC 13-046 Diesel Generator Vent Line Tornado Missile Durability
: Attachment 2
: The following items are requested for the Occupational/Public Radiation Safety Inspection at Cooper Station
(March 21
-24, 2016)
: Integrated Report 2016001
: Inspection areas are listed in the attachments below.
: Please provide the requested information on or before Monday, February 29, 2016.
: Please submit this information using the same lettering system as below.
: For example, all contacts and phone numbers for Inspection Procedure 71124.01 should be in a file/folder titled
"1- A," applicable organization charts in file/folder "1
- B," etc.
: If information is placed on ims.certrec.com, please ensure the inspection exit date entered is at least 30 days later than the onsite inspection dates, so the inspectors will have access to the information while writing the report.
: In addition to the corrective action document lists provided for each inspection procedure listed below, please provide updated lists of corrective action documents at the entrance meeting.
: The dates for these lists should range from the end dates of the original lists to the day of th
e entrance meeting.
: More than one inspection procedure is to be conducted.
: Consequently, if the information requests appear to be redundant, there is no need to provide duplicate copies.
: Enter a note explaining in which file the information can be found
: If you have any questions or comments, please contact Martin J. Phalen at (817) 200
-1158 or Martin.Phalen@nrc.gov.
: PAPERWORK REDUCTION ACT STATEMENT
: This letter does not contain new or amended information collection requirements subject to the Paperwork Reduction Act of 1995 (44 U.S.C. 3501 et seq.). Existing information collection requirements were approved by the Office of Management and Budget, control number 3150
-0011.
: 2. Occupational ALARA Planning and Controls (71124.02)
: Date of Last Inspection:
: May 2015
: However, please provide information requested from January 1, 2015
, to present.
: A. List of contacts and telephone numbers for ALARA program personnel
. B. Applicable organization charts
. C. Copies of audits, self
-assessments, and LERs, written since date of last inspection
, focusing on ALARA
. D. Procedure index for ALARA Program
. E. Please provide specific procedures related to the following areas noted below.
: Additional specific procedures may be requested by number after the inspector reviews the procedure indexes.
: 1. ALARA Program
: 2. ALARA Committee
: 3. Radiation Work Permit Preparation
: F. A summary list of corrective action documents (including corporate and subtiered systems) written since date of last inspection
, related to the ALARA program.
: In addition to ALARA, the summary should also address radiation work permit (RWP) violations, electronic dosimeter alarms, and RWP dose estimates NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches
. G.
: List of work activities greater than 1 rem, since date of last inspection
.
: Include original dose estimate and actual dose.
: H. Site dose totals and 3
-year rolling averages for the past 3 years (based on dose of record). I. Outline of source term reduction strategy
. J. If available, provide
a copy of the ALARA outage report for the most recently completed outage. K. Please provide your most recent Annual ALARA Report.
: 4. Occupational Dose Assessment (Inspection Procedure 71124.04)
: Date of Last Inspection:
: June 2014
: However, please provide information requested from January 1, 2014
, to present.
: A. List of contacts and telephone numbers for the following areas:
: Dose Assessment personnel
: B. Applicable organization charts
: C. Audits, self
-assessments, vendor or NUPIC audits of contractor support, and LERs written since date of last inspection, related to:
: Occupational Dose Assessment
: D. Procedure indexes for the following areas
: Occupational Dose Assessment
: E. Please provide specific procedures related to the following areas noted below.
: Additional specific procedures will be requested by number after the inspector reviews the procedure indexes.
: 1. Radiation Protection Program
: 2. Radiation Protection Conduct of Operations
: 3. Personnel Dosimetry Program
: 4. Radiological Posting and Warning Devices
: 5. Air Sample Analysis
: 6. Performance of High Exposure Work
: 7. Declared Pregnant Worker
: 8. Bioassay Program
: F. List of corrective action documents (including corporate and subtiered systems) written since date of last inspection
, associated with:
: 1. National Voluntary Laboratory Accreditation Program (NVLAP)
: 2. Dosimetry (TLD/OSL, etc.) problems
: 3. Electronic alarming dosimeters
: 4. Bioassays or internally deposited radionuclides or internal dose
: 5. Neutron dose
: NOTE: The lists should indicate the significance level of each issue and the search criteria used.
: Please provide in document formats which are "searchable" so that the inspector can perform word searches.
: G. List of positive whole body counts since date of last inspection, names redacted if desired. H. Part 61 analyses/scaling factors
. I The most recent NVLAP
accreditation report or, if dosimetry is provided by a vendor, the vendor's most recent results
.
}}
}}

Latest revision as of 00:38, 10 January 2025

NRC Integrated Inspection Report 05000298/2016001
ML16119A441
Person / Time
Site: Cooper Entergy icon.png
Issue date: 04/28/2016
From: Greg Warnick
NRC/RGN-IV/DRP/RPB-C
To: Limpias O
Nebraska Public Power District (NPPD)
Warnick G
References
EA-15-089 IR 2016001
Download: ML16119A441 (45)


Text

April 28, 2016

SUBJECT:

COOPER NUCLEAR STATION - NRC INTEGRATED INSPECTION REPORT 05000298/2016001

Dear Mr. Limpias:

On March 31, 2016, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Cooper Nuclear Station. On April 8, 2016, the NRC inspectors discussed the results of this inspection with you and other members of your staff. Inspectors documented the results of this inspection in the enclosed inspection report.

NRC inspectors documented two findings of very low safety significance (Green) in this report.

Both of these findings involved violations of NRC requirements. The NRC is treating these violations as non-cited violations (NCVs) consistent with Section 2.3.2.a of the NRC Enforcement Policy.

If you contest the violations or significance of these NCVs, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident inspector at the Cooper Nuclear Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a response within 30 days of the date of this inspection report, with the basis for your disagreement, to the Regional Administrator, Region IV; and the NRC resident inspector at the Cooper Nuclear Station.

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your response (if any) will be available electronically for public inspection in the NRCs Public Document Room or from the Publicly Available Records (PARS) component of the NRC's Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Gregory G. Warnick, Chief Project Branch C Division of Reactor Projects

Docket No. 50-298 License No. DPR-46

Enclosure:

Inspection Report 05000298/2016001 w/ Attachment:

1. Supplemental Information 2. Request for Information for the O

REGION IV==

Docket:

05000298 License:

DPR-46 Report:

05000298/2016001 Licensee:

Nebraska Public Power District Facility:

Cooper Nuclear Station Location:

72676 648A Ave Brownville, NE Dates:

January 1 through March 31, 2016 Inspectors: P. Voss, Senior Resident Inspector C. Henderson, Resident Inspector W. Sifre, Senior Reactor Inspector M. Phalen, Senior Health Physicist J. ODonnell, CHP, Health Physicist Approved By:

Greg Warnick Chief, Project Branch C Division of Reactor Projects

- 2 -

SUMMARY

IR 05000298/2016001; 01/01/2016 - 03/31/2016; Cooper Nuclear Station; Surveillance Testing.

The inspection activities described in this report were performed between January 1 and March 31, 2016, by the resident inspectors at the Cooper Nuclear Station and inspectors from the NRCs Region IV office. Two findings of very low safety significance (Green) are documented in this report. Both of these findings involved violations of NRC requirements. The significance of inspection findings is indicated by their color (Green, White, Yellow, or Red), which is determined using Inspection Manual Chapter 0609, Significance Determination Process. Their cross-cutting aspects are determined using Inspection Manual Chapter 0310,

Aspects within the Cross-Cutting Areas. Violations of NRC requirements are dispositioned in accordance with the NRC Enforcement Policy. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process.

Cornerstone: Mitigating Systems

Green.

The inspectors identified a non-cited violation of 10 CFR 50.55a, Codes and Standards, for the licensees failure to follow the ASME Code for Operation and Maintenance of Nuclear Power Plants when addressing the performance of reactor equipment cooling pump A within the high required action range of the inservice testing program. Specifically, on February 11, 2016, the licensee failed to follow ASME Subsection ISTB 6200(b) when engineering personnel, taking corrective action to address pump performance, failed to either correct the cause of the deviation or establish new reference values for the pump. Instead of establishing new reference values, the licensee performed an analysis to administratively raise the upper required action range limit, creating a wider range of acceptable pump operation than allowed by Table ISTB-5100-1, Centrifugal Pump Test Acceptance Criteria. The licensee entered this issue into the corrective action program as Condition Report CR-CNS-2016-00920, took action to reevaluate and rebaseline the pump with new reference values, and performed an extent of condition review to determine if other equipment was impacted by similar interpretations of the code.

The licensees failure to establish new reference values for reactor equipment cooling pump A in accordance with the ASME Code was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the human performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the actions initially taken by the licensee would have required a relief request; could have delayed identification of a degrading pump trend due to the creation of a wider range of acceptable operation; and the licensees generic interpretation, that the Table ISTB-5100-1 acceptable range could be administratively expanded, represented a programmatic vulnerability. The inspectors used Manual Chapter 0609,

Appendix A, The Significance Determination Process (SDP) for Findings At-Power, and determined that the finding had very low safety significance (Green) because it did not represent a design or qualification deficiency, did not represent a loss of safety function for a single train for greater than its technical specification allowed outage time, and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. This finding had a cross-cutting aspect in the area of problem identification and resolution associated with evaluation. Specifically, the licensee failed to thoroughly evaluate performance of reactor equipment cooling pump A in the required action range to ensure that the resolution correctly addressed the causes of the degraded performance [P.2].

(Section 1R22)

Cornerstone: Barrier Integrity

Green.

The inspectors identified a non-cited violation of Technical Specification 5.4.1.a, for the licensees failure to follow Station Procedure 0.26, Surveillance Program, and assess the operability of high pressure coolant injection steam line isolation instrumentation during surveillance testing. Specifically, the licensee failed to assess the operability of required isolation instrumentation when maintentance personnel opened terminal box 392 during surveillance testing and temporarily invalidated its environmental qualification. Licensee procedures required operations personnel to either establish compensatory measures to restore the terminal box during an event, or declare the instrumentation inoperable and enter the applicable technical specification actions when the terminal box was opened. As an immediate corrective action, the licensee implemented Standing Order 2016-03, which directed operators to establish compensatory measures, if applicable, or declare the affected equipment inoperable when environmentally qualified terminal boxes would be opened during testing. The licensee entered this issue into their corrective action program for resolution as Condition Reports CR-CNS-2016-00320 and CR-CNS-2016-00476.

The licensees failure to assess the operability of high pressure coolant injection instrumentation when the associated terminal box was opened during surveillance testing, in violation of Station Procedure 0.26, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the structure, system, component, and barrier performance attribute of the Barrier Integrity Cornerstone, and adversely affected the cornerstone objective to ensure the radiological barrier functionality of containment isolation. Specifically, with terminal box 392 open, its environmental qualification was temporarily invalidated, making the high pressure coolant injection low steam pressure and high steam flow containment isolation instrumentation inoperable during surveillance testing. In addition, two other terminal boxes and their associated surveillances were impacted by the performance deficiency. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, the inspectors determined that the finding had very low safety significance (Green) because it: (1) did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components; and (2) did not involve an actual reduction in function of hydrogen igniters in the reactor containment. The finding had a cross-cutting aspect in the area of human performance associated with work management. Specifically, the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority, including the identification and management of risk commensurate with opening terminal box 392 during surveillance testing [H.5].

(Section 1R22)

PLANT STATUS

The Cooper Nuclear Station began the inspection period at full power. On February 12, 2016, the licensee lowered reactor power to approximately 70 percent in order to perform surveillance testing and planned work on reactor feedwater pump B. The plant returned to full power on February 13, 2016, where it remained for the rest of the reporting period, except for minor reductions in power to support scheduled surveillance testing and rod pattern adjustments.

REPORT DETAILS

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R04 Equipment Alignment

.1 Partial Walkdown

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant systems:

  • February 19, 2016, Service water cross connect valves SW-MOV-36 and SW-MOV-37 and design flow requirements
  • February 29, 2016, Diesel generator sequential loading and kW loading analysis
  • March 23, 2016, Instrument air system and reactor equipment cooling The inspectors reviewed the licensees procedures and system design information to determine the correct lineup for the systems. They visually verified that critical portions of the systems were correctly aligned for the existing plant configuration.

These activities constituted four partial system walkdown samples, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

.2 Complete Walkdown

a. Inspection Scope

On March 8, 2016, the inspectors performed a complete system walkdown inspection of the residual heat removal service water system. The inspectors reviewed the licensees procedures and system design information to determine the correct system lineup for the existing plant configuration. The inspectors also reviewed outstanding work orders, open condition reports, in-process design changes, temporary modifications, and other open items tracked by the licensees operations and engineering departments. The inspectors then visually verified that the system was correctly aligned for the existing plant configuration.

These activities constituted one complete system walkdown sample, as defined in Inspection Procedure 71111.04.

b. Findings

No findings were identified.

1R05 Fire Protection

Quarterly Inspection

a. Inspection Scope

The inspectors evaluated the licensees fire protection program for operational status and material condition. The inspectors focused their inspection on four plant areas important to safety:

  • January 11, 2016, Reactor feed pumps area, Fire Area TB-A, Zone 11E
  • February 24, 2016, Diesel generator room 1, Fire Area DG-A, Zone 14A and 14C
  • February 24, 2016, Diesel generator room 2, Fire Area DG-B, Zone 14B and 14D
  • March 3, 2016, Auxiliary relay room, Fire Area CB-D, Zone 8A

For each area, the inspectors evaluated the fire plan against defined hazards and defense-in-depth features in the licensees fire protection program. The inspectors evaluated control of transient combustibles and ignition sources, fire detection and suppression systems, manual firefighting equipment and capability, passive fire protection features, and compensatory measures for degraded conditions.

These activities constituted four quarterly inspection samples, as defined in Inspection Procedure 71111.05.

b. Findings

No findings were identified.

1R06 Flood Protection Measures

a. Inspection Scope

On February 29, 2016, the inspectors completed an inspection of the stations ability to mitigate flooding due to internal causes. After reviewing the licensees flooding analysis, the inspectors chose one plant area containing risk-significant structures, systems, and components that were susceptible to flooding:

  • Control building basement The inspectors reviewed plant design features and licensee procedures for coping with internal flooding. The inspectors walked down the selected area to inspect the design features, including the material condition of seals, drains, and flood barriers. The inspectors evaluated whether operator actions credited for flood mitigation could be successfully accomplished.

These activities constituted completion of one flood protection measures sample, as defined in Inspection Procedure 71111.06.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

.1 Review of Licensed Operator Requalification

a. Inspection Scope

On February 19, 2016, the inspectors observed an evaluated simulator scenario performed by an operating crew. The inspectors assessed the performance of the operators and the evaluators critique of their performance. The inspectors also assessed the modeling and performance of the simulator during the requalification activities.

These activities constituted completion of one quarterly licensed operator requalification program sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

.2 Review of Licensed Operator Performance

a. Inspection Scope

On February 13, 2016, the inspectors observed the performance of on-shift licensed operators in the plants main control room. At the time of the observations, the plant was in a period of heightened activity due to maintenance and testing associated with a planned downpower to 70 percent. The inspectors observed the operators performance of the following activities:

  • Rod manipulations associated with the downpower and rod pattern change, including the pre-job brief

In addition, the inspectors assessed the operators adherence to plant procedures, including conduct of operations procedure and other operations department policies.

These activities constituted completion of one quarterly licensed operator performance sample, as defined in Inspection Procedure 71111.11.

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed two instances of degraded performance or condition of safety-related or risk-significant structures, systems, and components (SSCs):

  • February 29, 2016, Core spray reference leg injection
  • January 19, 2016, Reactor recirculation motor generator sets

The inspectors reviewed the extent of condition of possible common cause SSC failures and evaluated the adequacy of the licensees corrective actions. The inspectors reviewed the licensees work practices to evaluate whether these may have played a role in the degradation of the SSCs. The inspectors assessed the licensees characterization of the degradation in accordance with 10 CFR 50.65 (the Maintenance Rule), and verified that the licensee was appropriately tracking degraded performance and conditions in accordance with the Maintenance Rule.

These activities constituted completion of two maintenance effectiveness samples, as defined in Inspection Procedure 71111.12.

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed four risk assessments performed by the licensee prior to changes in plant configuration and the risk management actions taken by the licensee in response to elevated risk:

  • March 25, 2016, Diesel generator system maintenance window, Division II The inspectors verified that these risk assessments were performed timely and in accordance with the requirements of 10 CFR 50.65 (the Maintenance Rule) and plant procedures. The inspectors reviewed the accuracy and completeness of the licensees risk assessments and verified that the licensee implemented appropriate risk management actions based on the result of the assessments.

The inspectors also observed portions of two emergent work activities that had the potential to affect the functional capability of mitigating systems or to impact barrier integrity:

  • January 19, 2016, Diesel generator 1 repairs due to frequency starting time greater than technical specification surveillance requirements
  • January 29, 2016, Loss of plant monitoring and information system/Gardel power supplies The inspectors verified that the licensee appropriately developed and followed a work plan for these activities. The inspectors verified that the licensee took precautions to minimize the impact of the work activities on unaffected structures, systems, and components.

These activities constituted completion of six maintenance risk assessment and emergent work control inspection samples, as defined in Inspection Procedure 71111.13.

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments

a. Inspection Scope

The inspectors reviewed five operability determinations that the licensee performed for degraded or nonconforming structures, systems, or components (SSCs):

  • March 25, 2016, Operability determination of service water due to inconsistent pump column minimum wall thickness acceptance criteria, CR-CNS-2016-01448 The inspectors reviewed the timeliness and technical adequacy of the licensees evaluations. Where the licensee determined the degraded SSC to be operable, the inspectors verified that the licensees compensatory measures were appropriate to provide reasonable assurance of operability. The inspectors verified that the licensee had considered the effect of other degraded conditions on the operability of the degraded SSC.

On January 25, 2016, the inspectors completed their review of operator actions taken or planned to compensate for degraded or nonconforming conditions. The inspectors verified that the licensee effectively managed these operator workarounds to prevent adverse effects on the function of mitigating systems and to minimize their impact on the operators ability to implement abnormal and emergency operating procedures.

These activities constituted completion of six operability and functionality review samples, which included one operator work-around sample, as defined in Inspection Procedure 71111.15.

b. Findings

No findings were identified.

1R18 Plant Modifications

a. Inspection Scope

On March 9, 2016, the inspectors reviewed a permanent plant modification associated with the replacement of safety-related General Electric magne blast breakers with Siemens horizontal vacuum bottle circuit breakers which affected risk-significant structures, systems, and components (SSCs).

The inspectors reviewed the design and implementation of the modification. The inspectors verified that work activities involved in implementing the modification did not adversely impact operator actions that may be required in response to an emergency or other unplanned event. The inspectors verified that post-modification testing was adequate to establish the operability of the SSCs as modified.

These activities constituted completion of one sample of permanent modifications, as defined in Inspection Procedure 71111.18.

b. Findings

No findings were identified.

1R19 Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed six post-maintenance testing activities that affected risk-significant structures, systems, or components (SSCs):

  • January 19, 2016, Diesel generator 1 emergent work
  • February 19, 2016, Torus to reactor vacuum breaker control switch replacement The inspectors reviewed licensing-and design-basis documents for the SSCs and the maintenance and post-maintenance test procedures. The inspectors observed the performance of the post-maintenance tests to verify that the licensee performed the tests in accordance with approved procedures, satisfied the established acceptance criteria, and restored the operability of the affected SSCs.

These activities constituted completion of six post-maintenance testing inspection samples, as defined in Inspection Procedure 71111.19.

b. Findings

No findings were identified.

1R22 Surveillance Testing

a. Inspection Scope

The inspectors observed six risk-significant surveillance tests and reviewed test results to verify that these tests adequately demonstrated that the structures, systems, and components (SSCs) were capable of performing their safety functions:

In-service tests:

  • January 26, 2016, Service water quarterly and post-loss of coolant accident flow surveillance acceptance criteria
  • February 9, 2016, Diesel generator 31 day operability test, Division I
  • February 19, 2016, Reactor equipment cooling pump A inservice testing surveillance
  • March 3, 2016, SW-MOV-36 and SW-MOV-37 surveillance testing The inspectors verified that these tests met technical specification requirements, that the licensee performed the tests in accordance with their procedures, and that the results of the tests satisfied appropriate acceptance criteria. The inspectors verified that the licensee restored the operability of the affected SSCs following testing.

These activities constituted completion of six surveillance testing inspection samples, as defined in Inspection Procedure 71111.22.

b. Findings

(1) Failure to Follow ASME Code Requirements when taking Corrective Actions for a Pump in the Required Action Range
Introduction.

The inspectors identified a Green, non-cited violation of 10 CFR 50.55a, Codes and Standards, for the licensees failure to follow the ASME Code for Operation and Maintenance of Nuclear Power Plants (OM) when addressing the performance of reactor equipment cooling (REC) pump A within the high required action range of the inservice testing program. Specifically, the licensee failed to follow ASME Subsection ISTB-6200(b) when engineering personnel, while taking corrective action to address pump performance, failed to either correct the cause of the deviation or establish new reference values for the pump.

Description.

On February 11, 2016, the licensee performed Surveillance Procedure 6.1REC.101, REC Surveillance Operation (IST) - Div 1, for the two-year comprehensive inservice test (IST) of REC pump A. This procedure was being used to meet the IST requirements for the pump in accordance with the 2001 Edition through the 2003 Addenda of the ASME OM Code. During the IST, the pump exceeded the upper limit for discharge pressure required by the test, which put the pump in the high required action range in accordance with the ASME Code. Consistent with the surveillance procedure and ASME OM Subsection ISTB-6200(b), the licensee declared the pump inoperable upon discovery of the condition. The licensee initiated condition report CR-CNS-2016-00784 to document the unacceptable inservice test results for REC pump A.

ASME Section ISTB-6200, Corrective Action, Subsection (b), states, If the measured test parameter values fall within the required action range of Table ISTB-5100-1, the pump shall be declared inoperable until either the cause of the deviation has been determined and the condition is corrected, or an analysis of the pump is performed and new reference values are established in accordance with ISTB-6200(c). The licensee determined that the pump was operating acceptably, and as a result, determined that there was no need to correct the cause of the deviation in pump performance. However, the licensee did not establish new reference values, which serve to provide a baseline of acceptable pump performance, in accordance with ISTB-6200(c). Instead, engineering personnel performed an analysis which assessed the operational readiness of the pump and evaluated pump performance trends as discussed in ISTB-6200(c), but rather than rebaseline the pump, the licensee administratively raised the upper required action limit. Following this action, operations personnel declared REC pump A operable.

The inspectors reviewed the licensees actions and challenged the sites decision to neither correct nor rebaseline the pump in accordance with Subsection ISTB-6200(b).

The inspectors observed that the licensees actions to raise the upper required action limit inappropriately created a wider range of acceptable pump operation than allowed by ASME Table ISTB-5100-1, Centrifugal Pump Test Acceptance Criteria. In consultation with NRC regional and headquarters ASME Code experts, the inspectors concluded that these actions put the site in nonconformance with the ASME Code. The inspectors observed that the licensees change would have required an NRC relief request and could have delayed identification of a degrading pump trend due to the creation of a wider range of acceptable operation. In response to inspector questions, the licensee determined that they had used this same method for different equipment on previous occasions. The inspectors determined that the licensees generic interpretation that Table ISTB-5100-1 acceptance criteria multipliers could be changed using Subsection ISTB-6200 represented a potential programmatic vulnerability. This issue was entered into the licensees corrective action program as CR-CNS-2016-00920, and the licensee subsequently took corrective action to establish new reference values for the pump.

Analysis.

The licensees failure to establish new reference values for REC pump A in accordance with the ASME OM code was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the human performance attribute of the Mitigating Systems Cornerstone, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the actions initially taken by the licensee would have required a relief request; could have delayed identification of a degrading pump trend due to the creation of a wider range of acceptable operation; and the licensees generic interpretation that the Table ISTB-5100-1 acceptable range could be administratively expanded represented a programmatic vulnerability. The inspectors used Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, and determined that the finding had very low safety significance (Green) because it did not represent a design or qualification deficiency, did not represent a loss of safety function for a single train for greater than its technical specification allowed outage time, and did not screen as potentially risk significant due to a seismic, flooding, or severe weather initiating event. This finding had a cross-cutting aspect in the area of problem identification and resolution associated with evaluation. Specifically, the licensee failed to thoroughly evaluate performance of REC pump A in the required action range to ensure that the resolution correctly addressed the causes of the degraded performance [P.2].

Enforcement.

Title 10 of the Code of Federal Regulations, Section 50.55a(b), Codes and Standards, requires, in part, that systems and components of boiling and pressurized water cooled nuclear power reactors must meet the requirements of the ASME Code for Operation and Maintenance of Nuclear Power Plants. Contrary to the above, on February 11, 2016, the licensee failed to ensure that systems and components in the plant met the requirements of the ASME OM Code. Specifically, the licensee failed to ensure ASME Subsection ISTB 6200(b) was met when engineering personnel, while taking corrective action to address REC pump A performance, failed to either correct the cause of the deviation or establish new reference values for the pump.

Upon discovery, the licensee took action to reevaluate and rebaseline the pump with new reference values, and performed an extent of condition review to determine if other equipment was impacted by similar interpretations of the code. This violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy, because it was of very low safety significance (Green) and was entered into the licensees corrective action program as Condition Report CR-CNS-2016-00920.

(NCV 05000298/2016001-01, Failure to Follow ASME Code Requirements when taking Corrective Actions for a Pump in the Required Action Range)

(2) Failure to Assess Operability of Technical Specification System Functions during Surveillance Testing
Introduction.

The inspectors identified a Green, non-cited violation of Technical Specification (TS) 5.4.1.a, for the licensees failure to follow Station Procedure 0.26, Surveillance Program, and assess the operability of high pressure coolant injection (HPCI) steam line isolation instrumentation during surveillance testing. Specifically, the licensee failed to assess the operability of required HPCI isolation instrumentation when maintenance personnel opened terminal box (TB) 392 during surveillance testing and temporarily invalidated its environmental qualification.

Description.

On January 14, 2016, the inspectors observed surveillance testing for the Division 1 HPCI low steam pressure containment isolation function for HPCI-MOV-15 in accordance with Station Procedure 6.1HPCI.701, HPCI Steam Line Low Pressure Channel Functional Test (DIV 1), Revision 5, under Work Order 5022860. During the surveillance test the inspectors identified that the licensee opened TB 392 to conduct the surveillance test. This terminal box was identified as environmentally qualified (EQ).

The inspectors questioned if TB 392 was EQ in the open condition during the surveillance test. Following a review of documentation for the terminal box, the inspectors determined that TB 392 was only EQ in the closed condition in accordance with drawing CNS-EQ-122, Sheet 1 and Sheet 2, Cooper Nuclear Station EQ Configuration Detail Terminal Boxes and Equipment Enclosures, Revision 6 and Revision 5. Drawing CNS-EQ-122, Sheet 1 and Sheet 2, stated that the enclosure for TB 392 was credited with protecting terminal blocks from direct exposure to high-energy line break (HELB) conditions and did not contain the field wires and Raychem splices that would allow the instrumentation to be EQ without an enclosure.

Station Procedure 0.26, Surveillance Program, Revision 68, Section 5 and Discussion Section 1.6 required the licensee to assess operability of TS system functions during surveillance testing, and stated that delayed entry was only allowed if there was not a loss of function. Section 5 of this procedure stated, the Shift Manager shall: be aware of any other systems affected by the test and how they are affected. Discussion Section 1.6 stated, TS requirements may have notes that allow delayed entry into conditions and required actions for equipment made inoperable by performance of the surveillance. Even though delayed entry is allowed, the equipment/component is still considered inoperable while performing these surveillances. The delayed entry is only allowed if there is not a loss of function. Additionally, Station Procedure 0-Barrier, Barrier Control Process, Revision 21, stated that opening terminal boxes in the reactor building required that either a compensatory measure be put in place or the SSC be declared inoperable.

The station did not implement a compensatory measure or declare instrumentation in the TB inoperable. The inspectors and licensee concluded that the shift manager should have been aware of the impacts of opening the TB, and in accordance with procedures, should have declared the TS system function inoperable for the HPCI low steam pressure and HPCI high steam flow isolation instrumentation when TB 392 was opened.

Therefore, usage of the six hour delayed entry time for TS 3.3.6.1, Primary Containment Isolation Instruments, was not allowed per Procedure 0.26 due to the instruments not being inoperable solely for surveillance testing. As immediate corrective actions, the licensee identified additional TBs impacted by this concern, and implemented Standing Order 2016-03, which directed operators to either establish compensatory measures or declare the affected equipment inoperable when EQ TBs would be opened during testing. The licensee created long term corrective actions to assess whether compensatory measures could be justified for TBs opened during surveillance testing in the reactor building, to assess whether open TBs could be qualified, and to update station procedures as required. The license entered this deficiency into their corrective action program for resolution as Condition Reports CR-CNS-2016-00320 and CR-CNS-2016-00476.

Analysis.

The licensees failure to assess the operability of HPCI isolation instrumentation when the associated terminal box was opened during surveillance testing, in violation of Station Procedure 0.26, was a performance deficiency. The performance deficiency was determined to be more than minor, and therefore a finding, because it was associated with the SSC and barrier performance attribute of the Barrier Integrity Cornerstone, and adversely affected the cornerstone objective to ensure the radiological barrier functionality of containment isolation. Specifically, with terminal box 392 open, its environmental qualification was temporarily invalidated, making the HPCI isolation instrumentation inoperable during surveillance testing. In addition, two other terminal boxes and their associated surveillances were impacted by the performance deficiency. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green)because it:

(1) did not represent an actual open pathway in the physical integrity of reactor containment, containment isolation system, or heat removal components; and
(2) did not involve an actual reduction in function of hydrogen igniters in the reactor containment. The finding had a cross-cutting aspect in the area of human performance associated with work management. Specifically, the licensee failed to implement a process of planning, controlling, and executing work activities such that nuclear safety was the overriding priority, including the identification and management of risk commensurate with opening terminal box 392 during surveillance testing [H.5].
Enforcement.

Technical Specification 5.4.1.a, requires, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix A to Regulatory Guide 1.33, Quality Assurance Program Requirements, of February 1978. Section 1.f of Appendix A to Regulatory Guide 1.33 requires specific procedures for scheduling surveillance tests and calibration. The licensee established Station Procedure 0.26, Surveillance Program, Revision 68, to schedule and control surveillance testing. Section 5 of Station Procedure 0.26 states, the Shift Manager shall: be aware of any other systems affected by the test and how they are affected. Contrary to the above, on January 14, 2016, the licensee failed to ensure that the shift manager was aware of any other systems affected by the test and how they were affected during HPCI isolation surveillance testing. Specifically, the licensee failed to assess the operability of all affected containment isolation instrumentation when maintenance personnel opened TB 392 during surveillance testing and temporarily invalidated its environmental qualification. As immediate corrective actions, the licensee identified additional TBs impacted by the performance deficiency, and implemented Standing Order 2016-03, which directed operators to either establish compensatory measures or declare the affected equipment inoperable when environmentally qualified TB would be opened during testing. This violation is being treated as a non-cited violation, consistent with Section 2.3.2.a of the Enforcement Policy, because it was of very low safety significance (Green) and was entered into the licensees corrective action program as Condition Reports CR-CNS-2016-0320 and CR-CNS-2016-00476. (NCV 05000298/2016001-02, Failure to Assess Operability of Technical Specification System Functions during Surveillance Testing)

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

Emergency Preparedness Drill Observation

a. Inspection Scope

The inspectors observed an emergency preparedness drill on March 29, 2016, to verify the adequacy and capability of the licensees assessment of drill performance. The inspectors reviewed the drill scenario, observed the drill from the Technical Support Center (TSC) and Simulator, and attended the post-drill critique. The inspectors verified that the licensees emergency classifications, off-site notifications, and protective action recommendations were appropriate and timely. The inspectors verified that any emergency preparedness weaknesses were appropriately identified by the licensee in the post-drill critique and entered into the corrective action program for resolution.

These activities constituted completion of one emergency preparedness drill observation sample, as defined in Inspection Procedure 71114.06.

b. Findings

No findings were identified.

RADIATION SAFETY

Cornerstones: Public Radiation Safety and Occupational Radiation Safety

2RS2 Occupational ALARA Planning and Controls

a. Inspection Scope

The inspectors assessed licensee performance with respect to maintaining individual and collective radiation exposures as low as is reasonably achievable (ALARA). The inspectors performed this portion of the attachment as a post-outage review. During the inspection the inspectors interviewed licensee personnel, reviewed licensee documents, and evaluated licensee performance in the following areas:

  • Radiological work planning, including work activities of exposure significance, and radiological work planning ALARA evaluations, initial and revised exposure estimates, and exposure mitigation requirements. The inspectors also verified that the licensees planning identified appropriate dose reduction techniques, reviewed any inconsistencies between intended and actual work activity doses, and determined if post-job (work activity) reviews were conducted to identify lessons learned. Specific work plans reviewed included refuel floor activities for the refuel bridge upgrades and radwaste processing for High-Integrity Container (HIC) preparations for shipping.
  • Verification of dose estimates and exposure tracking systems including the basis for exposure estimates, and measures to track, trend, and if necessary reduce occupational doses for ongoing work activities. The inspectors evaluated the licensees method for adjusting exposure estimates and reviewed the licensees evaluations of inconsistent or incongruent results from the licensees intended radiological outcomes.
  • Problem identification and resolution for ALARA planning and controls. The inspectors reviewed audits, self-assessments, work-in-progress and post-job ALARA reviews, and corrective action program documents to verify problems were being identified and properly addressed for resolution.

These activities constituted completion of two of the five required samples of occupational ALARA planning and controls, as defined in Inspection Procedure 71124.02.

b. Findings

No findings were identified.

2RS4 Occupational Dose Assessment

a. Inspection Scope

The inspectors evaluated the accuracy and operability of the licensees personnel monitoring equipment, verified the accuracy and effectiveness of the licensees methods for determining total effective dose equivalent, and verified that the licensee was appropriately monitoring occupational dose. The inspectors interviewed licensee personnel, walked down various portions of the plant, and reviewed licensee performance in the following areas:

  • Source term characterization, including characterization of radiation types and energies, hard-to-detect isotopes, and scaling factors.
  • External dosimetry, including National Voluntary Laboratory Accreditation Program (NVLAP) accreditation, storage, issue, use, and processing of active and passive dosimeters.
  • The technical competency and adequacy of the licensees internal dosimetry program.
  • Adequacy of the dosimetry program for special dosimetry situations, such as declared pregnant workers, multiple dosimetry placement, effective dose equivalent for external exposures (EDEX), shallow dose equivalent, neutron dose assessment, and dose records.
  • Problem identification and resolution for occupational dose assessment, including audits, self-assessments, and corrective action documents.

These activities constituted completion of five occupational dose assessment inspection samples, as defined in Inspection Procedure 71124.04.

b. Findings

No findings were identified.

OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency Preparedness, Public Radiation Safety, Occupational Radiation Safety, and Security

4OA1 Performance Indicator Verification

.1 Unplanned Scrams per 7000 Critical Hours (IE01)

a. Inspection Scope

The inspectors reviewed licensee event reports (LERs) for the period of January 1 through December 31, 2015, to determine the number of scrams that occurred. The inspectors compared the number of scrams reported in these LERs to the number reported for the performance indicator. Additionally, the inspectors sampled monthly operating logs to verify the number of critical hours during the period. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the data reported.

These activities constituted verification of the unplanned scrams per 7000 critical hours performance indicator, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

.2 Unplanned Power Changes per 7000 Critical Hours (IE03)

a. Inspection Scope

The inspectors reviewed operating logs, corrective action program records, and monthly operating reports for the period of January 1 through December 31, 2015, to determine the number of unplanned power changes that occurred. The inspectors compared the number of unplanned power changes documented to the number reported for the performance indicator. Additionally, the inspectors sampled monthly operating logs to verify the number of critical hours during the period. The inspectors used definitions and guidance contained in Nuclear Energy Institute Document 99-02, Regulatory Assessment Performance Indicator Guideline, Revision 7, to determine the accuracy of the data reported.

These activities constituted verification of the unplanned power changes per 7000 critical hours performance indicator, as defined in Inspection Procedure 71151.

b. Findings

No findings were identified.

4OA2 Problem Identification and Resolution

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items entered into the licensees corrective action program and periodically attended the licensees condition report screening meetings. The inspectors verified that licensee personnel were identifying problems at an appropriate threshold and entering these problems into the corrective action program for resolution. The inspectors verified that the licensee developed and implemented corrective actions commensurate with the significance of the problems identified. The inspectors also reviewed the licensees problem identification and resolution activities during the performance of the other inspection activities documented in this report.

b. Findings

No findings were identified.

.2 Annual Follow-up of Selected Issues

a. Inspection Scope

The inspectors selected two issues for an in-depth follow-up:

  • On January 6, 2016, the inspectors reviewed entries in the control room log from the previous night shift, which discussed the identification of leakage into the scram discharge volume (SDV). Operations personnel had isolated the SDV in advance of performing planned maintenance on the system, in order to quantify any potential leakage into the SDV, if it existed. During this activity, operators determined that there was no leakage into the North SDV, but the South SDV indicated leakage accumulating at a rate of 5.2 inches per hour. The inspectors noted that this was an indication of scram outlet valve leakage, and also observed that no condition report (CR) was written for the leakage that was discovered. In response to inspector questions, operations personnel took action to initiate a CR (CR-CNS-2016-00075) and assess operability. The inspectors noted that the site had failed to meet the requirements of Step 5.3.6.3 of Procedure 0-CNS-LI-102, Corrective Action Process, which required, in part, that individuals ensure the condition was promptly documented on a Condition Report, by no later than the end of their shift.

In subsequent follow-up with the licensee, the inspectors learned that the CR had been considered a non-adverse condition, and as a result, CR generation had not been required. The CR had been classified as a D-trend non-adverse condition and closed. After further review, the inspectors determined that the condition met the licensee and NRC definition of a condition adverse to quality because the issue was a condition of an SSC, including failures and deficiencies, that could potentially render the SSC degraded or inoperable. Specifically, as discussed in GE SIL 173, a leaking scram [outlet] valve is of concern as the control rod drive (CRD) runs hot due to reactor water passing down through the drive and out the line to the scram discharge volume, and will continue to run hotter as the scram valve seat continues to erode. Eventually this could interfere with normal drive movement. In addition, the inspectors determined that scram outlet valve leakage into the SDV could result in high SDV water levels and undesirable scram signals if isolated, and could result in CRD drift if the leakage became excessive.

The inspectors determined that this issue represented a minor violation of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, which requires, in part, that activities affecting quality shall be accomplished in accordance with documented instructions, procedures, or drawings of a type appropriate to the circumstances. Licensee procedure 0-CNS-LI-102, Corrective Action Process, an Appendix B quality related procedure, provides instructions for identifying and classifying conditions adverse to quality. Procedure 0-CNS-LI-102, Attachment 1, states in part, that adverse conditions are required to be corrected in the Corrective Action Program (CAP)and are subject to the rigor necessary to evaluate and thoroughly resolve important and significant issues. Contrary to the above, between January 6, 2016, and March 17, 2016, the licensee failed to assure that an adverse condition was corrected in the CAP and was subject to the rigor necessary to evaluate and thoroughly resolve important and significant issues.

Specifically, the licensee initially failed to generate a condition report for indicated scram outlet valve leakage, and subsequently failed to classify the CR as a condition adverse to quality to ensure the deficiency would be resolved in the CAP. Instead, the CR was classified as D-Trend, which denotes a non-adverse condition that is handled outside of the CAP. The issue was minor in accordance with Inspection Manual Chapter 0612 Appendix B due to the minimal quantity of leakage identified and because other programmatic opportunities existed to identify the condition prior to significant plant impacts. Although this issue should be corrected, it constitutes a violation of minor significance that is not subject to enforcement action in accordance with Section 2 of the Enforcement Policy. The issue was entered into the licensees CAP as CR-CNS-2016-01485. Licensee investigation revealed one CRD with slightly elevated temperatures, and the licensee generated a work order to repair the associated scram outlet valve.

The inspectors assessed the licensees problem identification threshold and corrective actions to address the issue. The inspectors verified that the licensee appropriately prioritized the planned corrective actions and that these actions were adequate to correct the condition.

  • On January 11, 2016, the licensee identified that the Division 1 emergency diesel generator (EDG) was slow to start during a monthly surveillance test.

Specifically, the EDG achieved rated voltage and frequency in 14.2 seconds, which exceeded the surveillance requirement limit of 14 seconds. The delayed start was linked to a degraded shuttle valve in the non-safety portion of the air start system, which is normally bypassed during an emergency EDG start. The licensee determined that the apparent cause of the degradation was inadequate manufacturer controls of the component.

The inspectors assessed the licensees problem identification threshold, cause analyses, and extent of condition reviews. The inspectors verified that the licensee appropriately prioritized the corrective actions and that these actions were adequate to correct the condition.

These activities constituted completion of two annual follow-up samples as defined in Inspection Procedure 71152.

b. Findings

No findings were identified.

4OA5 Other Activities

(Closed) Notice of Violation 05000298/2015007-04, Failure to Evaluate the Lack of Missile Protection on the Emergency Diesel Generator 1 and 2 Fuel Oil Storage Tank Vents, EA-15-089 During the Component Design Basis Inspection conducted on April 6 through May 8, 2015, a violation of NRC regulations was identified and documented in NRC Inspection Report 05000298/2015007 (ML15173A450). The NRC had determined that a cited violation was associated with the inspection. The violation was cited because Cooper Nuclear Station (CNS) failed to restore compliance with NRC requirements within a reasonable amount of time after a previous violation was identified in NRC Inspection Report 05000298/2010007 (ML103370640).

In 2015, the team identified a Green, cited violation of 10 CFR Part 50, Appendix B, Criterion III, Design Control, which states, in part, Design control measures shall provide for verifying or checking the adequacy of design, such as by the performance of design reviews, by the use of alternate or simplified calculational methods, or by the performance of a suitable testing program. Specifically, the licensee failed to verify the adequacy of design of the vents for the emergency diesel generator (EDG) 1 and 2 fuel oil storage tanks to withstand impact from a tornado driven missile hazard, or to evaluate for exemption from missile protection requirements using an approved methodology.

The Notice of Violation (NOV) issued with the Inspection Report on June 22, 2015, required Cooper Nuclear Station to submit a written statement to the NRC within 30 days. The reply was required to contain the corrective steps taken to ensure full compliance was achieved. Cooper Nuclear Station submitted the response to the NRC on July 22, 2015 (ML15215A369). The corrective steps taken by the licensee included:

(1) incorporating a compilation of CNS and industry documentation into an engineering report to substantiate the conclusions of the design basis documents that evaluated the EDG fuel oil storage tank vents ability to perform their design function following a design basis missile strike;
(2) removing the cap on the storage tank fill opening and installing a screen to ensure operability per the associated work order;
(3) reinforcing with engineers qualified to prepare or review calculations, the need to explicitly and literally state the technical issues when performing calculations;
(4) incorporating lessons learned from the apparent cause evaluation as part of the Technical Rigor topic during engineering continuing training; and
(5) revising NEDC 13-046, Revision 1, to directly address all four tornado impact scenarios as described in Section XII, 2.3.3.2 of the CNS Updated Safety Analysis Report.

The NRC responded in a letter to Cooper Nuclear Stations response on August 11, 2015 (ML15224B562). The letter stated that the NRC would inform the licensee if further inspection was warranted. The inspector reviewed the licensees corrective actions associated with the violation. Specifically, the inspector reviewed Engineering Change EC-EE15-012, Diesel Generator Diesel Oil Tank Vents Tornado Missile Analysis, Revision 1, and Calculation NEDC 13-046, Diesel Generator Storage Vent Line Tornado Missile Durability, Revision 2. Based on this review, the inspector concluded that the licensee had performed adequate corrective actions to restore compliance, address extent of condition, and prevent recurrence. No additional deficiencies were identified during the review of this Notice of Violation.

This review closes NOV 05000298/2015007-04, Failure to Evaluate the Lack of Missile Protection on the Emergency Diesel Generator 1 and 2 Fuel Oil Storage Tank Vents, EA-15-089.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On March 24, 2016, the inspectors presented the results of the diesel fuel oil tank Notice of Violation closure review to Mr. D. Buman, Director of Engineering, and other members of the licensee staff via telephone. The licensee acknowledged the inspection results. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On March 24, 2016, the inspectors presented the radiation safety inspection results to Mr. K. Higginbotham, General Manager, Plant Operations, and other members of the licensee staff. The licensee acknowledged the inspection results. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

On April 8, 2016, the inspectors presented the inspection results to Mr. O. Limpias, Vice President and Chief Nuclear Officer, and other members of the licensee staff. The licensee acknowledged the issues presented. The licensee confirmed that any proprietary information reviewed by the inspectors had been returned or destroyed.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Barker, Manager, Engineering Program and Components
J. Bebb, Staff Health Physicist, Radiation Protection
D. Buman, Director, Engineering
B. Chapin, Manager, Maintenance
T. Chard, Manager, Quality Assurance
L. Dewhirst, Manager, Corrective Action and Assessment
K. Dia, Manager, System Engineering
J. Dixon, Supervisor, Radiation Protection
R. Estrada, Manager, Design Engineering
J. Flaherty, Senior Staff Engineer, Licensing
T. Forland, Engineer, Licensing
D. Goodman, Manager, Operations
K. Higginbotham, General Manager, Plant Operations
D. Kimball, Director, Nuclear Oversight
O. Limpias, Vice President, Chief Nuclear Officer
J. Olberding, Licensing Engineer, Regulatory Affairs
R. Penfield, Director, Nuclear Safety Assurance
J. Shaw, Manager, Licensing
J. Stough, Manager, Emergency Preparedness
C. Sunderman, Manager, Radiation Protection

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000298/2016001-01 NCV Failure to Follow ASME Code Requirements when taking Corrective Actions for a Pump in the Required Action Range (Section 1R22)
05000298/2016001-02 NCV Failure to Assess Operability of Technical Specification System Functions during Surveillance Testing (Section 1R22)

Closed

05000298/2015007-04 VIO Failure to Evaluate the Lack of Missile Protection on the Emergency Diesel Generator 1 and 2 Fuel Oil Storage Tank Vents (Section 4OA5)

LIST OF DOCUMENTS REVIEWED