IR 05000335/1997015: Difference between revisions

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{{Adams
{{Adams
| number = ML17229A580
| number = ML17229A597
| issue date = 01/02/1998
| issue date = 01/20/1998
| title = Responds to Violations Noted in Insp Repts 50-335/97-15 & 50-389/97-15.Corrective Actions:Completed Temporary Sys Alteration That Reversed Two of Three Power Leads to Low Speed Winding of Fan Motor at Motor Control Center
| title = Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-335/97-15 & 50-389/97-15
| author name = PLUNKETT T F
| author name = Landis K
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
| addressee name =  
| addressee name = Plunkett T
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
| addressee affiliation = FLORIDA POWER & LIGHT CO.
| docket = 05000335, 05000389
| docket = 05000335, 05000389
| license number =  
| license number =  
| contact person =  
| contact person =  
| document report number = 50-335-97-15, 50-389-97-15, L-97-322, NUDOCS 9801140201
| document report number = 50-335-97-15, 50-389-97-15, EA-97-501, NUDOCS 9802040144
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE
| title reference date = 01-02-1998
| page count = 9
| document type = CORRESPONDENCE-LETTERS, OUTGOING CORRESPONDENCE
| page count = 4
}}
}}


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{{#Wiki_filter:CATEGORY1REGULATORYINFORMATIONDISTRIBUTIONSYSTEM(RIDS)ACCESSIONNBR:9801140201DOC.DATE:98/01/02NOTARIZED:YESFACIL:50-335St.LuciePlant,Unit1,FloridaPowerEcLightCo.~~~~~~~-50-389St.LuciePlant,Unit2,FloridaPower&LightCo.AUTH.NAMEAUTHORAFFILIATIONPLUNKETT,T.F.FloridaPowertLightCo.RECZP.NAMERECIPIENTAFFILIATIONDocumentControlBranch(DocumentControlDesk)
{{#Wiki_filter:CATEGORY 2 v
REGULATORY INFORMATION.DISTRIBUTION SYSTEM (RXDS)
.'CCESSION NBR:9802040144'OC.DATE:.98/01/20>>
NOTARIZED: NO CIL':50'-335; St. Lucie Plant, Unit 1, Flori'da Power.


SUBJECT: Respondstoviolationsnotedininsprept50-335/97-15&50-389/97-15.Correctiveactions:completedtemporarysysalterationthatreversedtwoofthreepowerleadstolowspeedwindingoffanmotoratmotorcontrolcenter.DISTRIBUTIONCODE:IE01DCOPIESRECEIVED:LTRENCLSIZE:TITLE:General(50Dkt)-InspRept/NoticeofViolationResponseNOTES:DOCKET0500033505000389ERECIPIENTZDCODE/NAMEPD2-3PDNRR/DRPM/PECBNUDOCS-ABSTRACTOGC/HDS3XTERNAL:LITCOBRYCE,Q'NRCPDRCOPIESLTTRENCL112211111111111111RECIPIENTIDCODE/NAMEWIENS,L.AEOD/SPD/RABDEDRONRR/DRCH/HHFBNRR/DRPM/PERBOEDIRRGN2FILE01NOACNUDOCSFULLTEXTCOPIESLTTRENCL111111111111111111D0UNOTETOALL"RIDS"RECIPIENTS:PLEASEHELPUSTOREDUCEWASTE.TOHAVEYOURNAMEORORGANIZATIONREMOVEDFROMDISTRIBUTIONLISTSORREDUCETHENUMBEROFCOPIESRECEIVEDBYYOUORYOURORGANIZATION,CONTACTTHEDOCUMENTCONTROLDESK(DCD)ONEXTENSION415-2083TOTALNUMBEROFCOPIESREQUIRED:LTTR19ENCL19 FloridaPower5LightCompany.6351S.OceanDrive,JensenBeach,FL34957January2,1998L-97-32210CFR$2.201U.S.NuclearRegulatoryCommissionAttn:DocumentControlDeskWashington,D.C.20555Re:St.LucieUnits1and2DocketNos.50-335and50-389ReplytoaNoticeofViolationNRecialInsectionReort97-15FloridaPowerandLightCompany(FPL)hasreviewedthesubjectNoticeofViolationand,pursuantto10CFR$2.201,theresponsestotheviolationsareattached.FPLacknowledgesthatthecitedviolationsrelatedtotheinoperablecontainmentfancoolersareofsignificantregulatoryconcern.Asdescribedintheviolationresponse,FPLhastakencomprehensivecorrectiveactionstoresolvetheidentifiedcondition,andhasreviewedtheeventforgenericimplications.Inthiscontext,FPLappreciatesNRC'srecognitionofthequestioningattitudeexhibitedbySt.Luciepersonnelintheidentificationoftheinoperablecontainmentfancoolerandthetimelyandcomprehensivecorrectiveactionstaken.FPLisoptimisticthatthebehaviordemonstratedbythepersonnelthatidentifiedthefancoolertestingdeficiencyisindicativeoftheculturalchangesencouragedbySt.Luciemanagement.Pleasecontactuswithquestionsontheenclosedviolationresponses.Verytrulyyours,ThomasF.PlunkettPresidentNuclearDivisionTFP/JAS/EJWAttachmentcc:RegionalAdministrator,USNRC,RegionIISeniorResidentInspector,USNRC,St.LuciePlant980%140201980102PDRADOCKOS00033SPDRIIIIIIIIIIIII/IIIIIIIIIIIIIIII/IIIIIIIanFPLGroupcompany St.LucieUnits1and2~~~DocketNos.50-335and50-389L-97-322Page2STATEOFFLORIDA))COUNTYOFPALMBEACH)ss.ThomasF.Plunkettbeingfirstdulysworn,deposesandsays:ThatheisPresident,NuclearDivision,ofFloridaPower&LightCompany,theLicenseeherein;Thathehasexecutedtheforegoingdocument;thatthestatementsmadeinthisdocumentaretrueandcorrecttothebestofhisknowledge,informationandbelief,andthatheisauthorizedtoexecutethedocumentonbehalfofsaidLicensee.ThomasF.PlunkettSTATEOFFLORIDACOUNTYOFSworntoandsubscribedbeforemethis'dayof/~~M,1997byThomasF.Plunk6tt,whoisrsonallyknowntome.Name+go~~oridapIIYPOi&F'CiALtiOTARYSEALOi~COc":nNICnMGALINIS0OOuueaONRuuOSR)l~i)(IXICOidMSSIONEXPIRESOi:RPSFPT10,2001Print,typeorstampCommissionedNameofNotaryPublic)
& Li'ght Co.
L-97-322AttachmentP~g1~ViolaioATechnicalSpecification3.6.2.1statesthattwocontainmentspraytrainsandtwocontainmentcoolingtrainsshallbeOPERABLE.Contrarytotheabove,betweenMay16,1997andOctober8,1997,whileoperatinginModes1,2,and3,oneUnit2containmentcoolingtrainwasinoperable.R~g~ny1.FPLconcurswiththeviolation.2.REASONFORVIOLATIONThisviolationwascausedbyboth:a)personnelerrorduringpostmaintenancetestingactivitiesassociatedwithcontainmentcoolingfan2-HVS-1D;and,b)aninadequate31dayTechnicalSpecificationsurveillanceprocedure.Thesedeficienciescontributedtoreturningcontainmentcoolingfanunit2-HVS-1Dtoservicewhenitwasunabletoperformitsemergencymodeofoperationduetoreverseslowspeedoperation.CausesandcorrectiveactionsassociatedwiththeabovearediscussedinFPL'sresponsestoviolationsBandC,respectively.Thelowflowalarmfor2-HVS-1Dwasnotdocumentedduringtheperiodic18monthtestoftheengineeredsafetyfeaturesbecausethecontainmentfancoolerunitwasoutofserviceduringthetest.Althoughtheproceduralrequirementsfordocumentingactionstobetakentoresolveannunciatorsreceivedduringtheperformanceofsafeguardstestingwereweak,thistestwasnotamissedopportunityfordiscoveringthat2-HVS-1Dwasinoperableduringtheemergencymodeofoperation.3.CORRECTIVESTEPSTAKENANDTHERESULTSACHIEVEDFPLenteredtheapplicableTechnicalSpecificationACTIONstatementswhenthelowflowalarmswerereceivedduringinitialandsubsequentcontainmentfancoolerslowspeedtestingonOctober6andOctober7,1997.Thereverseslowspeedoperationwascorrectedbyimplementingatemporarysystemalterationthatreversedtwoofthethreepowerleadstothelowspeedwindingofthefanmotoratthemotorcontrolcenter.Thisactionwascompletedwithintheallowedoutagetimeforinoperablecontainmentfancooler(s).Containmentfancoolerunit2-HVS-1DwasreturnedtoserviceonOctober9,1997,afterproperoperationoftheunitwasverifie L-97-322AttachmentP~ae24.CORRECTIVESTEPSTOAVOIDFURTHERVIOLATIONSFPLrevisedsurveillanceoperatingprocedure1-0400050,"PeriodicTestoftheEngineeredSafetyFeatures,"toenhancethedispositionofannunciatorsthatarereceivedduringtheperformanceoftheIntegratedSafeguardsTest.Thisrevisionincludesanewappendixusedtotrackanddispositionannunciatorsthatoccurduringthetest.ThisrevisiontotheUnit1procedurewascompletedonNovember18,1997.B.TheUnit2Safeguardsprocedure,2-0400050,willberevisedtoincludethenewannunciatorresponseappendixpriortoperformingsafeguardstestingduringtheUnit21998refuelingoutage(SL2-11).FullcompliancewasachievedonOctober9,1997,whencontainmentfancoolerunit2-HVS-IDwasreturnedtoservic L-97-322AttachmentP~ae3VIolation810CFR50,AppendixB,CriterionV,Instructions,ProceduresandDrawings,requires,inpart,thatactivitiesaffectingqualityshallbeprescribedbydocumentedproceduresofatypeappropriatetothecircumstancesandshallbeaccomplishedinaccordancewiththoseprocedures.MaintenanceProcedure(MP)2-0950173,Revision9,"TheOverhaulofContainmentFanCoolersMotors2HVS-lA,1B,1C,1D(EQMotors),"Section9.9,implementsthepostmaintenancechecksofthecontainmentfancoolermotorsaftermaintenance.MP2-0950173requiresthefantobestartedinslowandfastspeedtoverifyproperbladerotationineachspeed.Contrarytotheabove,onMay16,1997,thelicenseefailedtoperformSection9.9ofMaintenanceProcedure2-0950173properlyinthatcontainmentfancooler2-HVS-1Dwasnotstartedinslowspeedandproperbladerotationwasnotverified.~Reaone1.FPLconcurswiththeviolation.REASONFORVIOLATIONThecausefortheviolationwaspersonnelerrorthatoccurredduringtheexecutionofpostmaintenancetestingperformedduringthelastUnit2refuelingoutage.Thiserrorresultedinreverserotationofcontainmentfancooler2-HVS-1D.TherootcauseevaluationconcludedthattheimpropertestexecutiononMay16,1997,wascausedbyfaultycommunicationsbetweenthemaintenancepersonnelassessingfanrotationinsidecontainmentandthecontrolroomoperatorwhostartedthefan.FPLreviewedthecompleteddocumentationfortheMay16,1997,postmaintenancetestandcompareditagainsttheMay16,1997,Unit2controlroomsequenceofeventsrecorder(SER).TheSERshowedthat2-HVS-1Dwasstartedtwiceduringthepostmaintenancetesting;however,boththeslowandfastspeedrotationalcheckswereperformedwiththemotoroperatinginfastspeed.Thefactthattwomotorstartsweredoneimpliesthatmaintenancepersonnelwerecorrectlyfollowingthetestproceduresteps.Theproperuseofthreewaycommunications,asrequiredbyboththeConductofMaintenanceandConductofOperationspolicies,wouldhavepreventedthefaultycommunicationwhichledtotheunsatisfactoryexecutionofthepostmaintenancetes L-97-322AttachmentP~ae43.CORRECTIVESTEPSTAKENANDTHERESULTSACHIEVEDA.ProcedureMP-2-0950173,"TheOverhaulofContainmentFanCoolerMotors2-HVS-lA,1B,1C,1D(EQMotors),"wasrevisedtorequirethefollowing:1)verificationsignaturesforbothfastandslowspeedmotorrotationtesting;2)acautionstatementtoensurethatbothwindingsareenergizedtoverifypropermotorrotationsubsequenttoelectricallyreconnectingthemotor;3)anaddendumsheetthatwillbeusedbythecontrolroomoperatorstofollowtheperformanceofthemotorrotationchecks;and,4)arequirementtoperformafunctionaltestofthecontainmentfancoolerinbothfastandslowspeedpriortoreturningtheunittoservice(i.e.,nolowflowalarmspresentduringrotationchecks).TheprocedurerevisionswerecompletedonNovember28,1997.AdditionaleditorialclarificationsweresubsequentlyaddedandapprovedonDecember17,1997.4.CORRECTIVESTEPSTOAVOIDFURTHERVIOLATIONSA.Thisspecificevent,includingtheimportanceofaccuratecommunicationsandtheuseofthreewaycommunications,wasincludedinaMaintenancetrainingbulletinthatwasissuedonNovember22,1997.B.ProcedureADM-78.01,"PostMaintenanceTesting,"willberevisedtoaddacautionnoteabouttestingmultiplespeedormultiplewindingmotorsbyJanuary31,1998.5.FullcompliancewasachievedonNovember28,1997,whentheprocedurerevisionstoMP-2-0950173,"TheOverhaulofContainmentFanCoolerMotors2-HVS-1A,1B,1C,1D(EQMotors),"werecomplete L-97-322AttachmentP~s5ViolationC10CFR50,AppendixB,CriterionXI,TestControl,requires,inpart,thatatestprogramshallbeestablishedtoassurethatalltestingrequiredtodemonstratethatcomponentswillperformsatisfactorilyinserviceisidentifiedandperformedinaccordancewithwrittentestprocedurewhichincorporatetherequirementsandacceptancelimitscontainedintheapplicabledesigndocuments.FinalSafetyAnalysisReportSection6.2.2.2.2statesthatthefancoolersoperateatareducedflowof39,600cubicfeetperminuteeach,withlowspeedmotoroperationduringaccidentoperation.NormalOperatingProcedure,NOP-2-2000020,Revision2,"ContainmentCoolingSystemOperation,"whichimplementsmonthlysurveillancetestingofthecontainmentfancoolers,requiresthateachcoolingtrainfanunitbestartedfromthecontrolroomandverifiedthateachunitoperatesforatleast15minutes,atleastonceper31days.Contrarytotheabove,asofOctober6,1997,thelicenseefailedtoassurethatalltestingrequiredtodemonstratethatcomponentswillperformsatisfactorilyinservice,inaccordancewiththerequirementsandacceptancelimitscontainedintheapplicabledesigndocuments,wasidentifiedandperformed.Specifically,NOP-2-2000020,didnotrequirethecontainmentcoolerfanstobetestedinslowspeed,whichisthealignmentrequiredduringemergencyoperation.Thisproceduralinadequacyhadexistedsinceinitialplantoperation.R~esense1.FPLconcurswiththeviolation.2.REASONFORVIOLATIONThecausefortheviolationwasnon-cognitivepersonnelerrorduringthedevelopmentofsurveillanceprocedureNOP2-2000020,"ContainmentCoolingSystemOperation,"thatresultedinthesurveillanceproceduredeficiency.Theprocedure,asitwaswritten,didnotmeettheintentoftheTechnicalSpecificationsurveillancerequirementsbecauseitrequiredtestingofthecontainmentcoolerfansonlyinthefastspeed,anddidnotrequireverificationofthepost-accidentsafetyrelatedfunctionofthefansinslowspee L-97-322AttachmentP~ae63.CORRECTIVESTEPSTAKENANDTHERESULTSACHIEVEDProcedureNOP2-2000020,"ContainmentCoolingSystemOperation,"wasrevisedandissuedonOctober13,1997.Therevisionclearlyrequiresthatallfansmustbestartedandruninslowspeed.Onceallfourfanshavebeenshiftedtoslowspeed,theabsenceofanylowflowalarmsthroughoutthe15minuteruntimeconstitutessatisfactorycompletionofthesurveillancetest.Theprocedurealsorequiressatisfactoryfastspeedoperationofthecontainmentfancoolers.B..FPLinvestigatedthegenericimplicationsofthiseventtodeterminewhatotherequipmenttypesmaybesubjecttoinadequatesurveillances.Thereviewrevealedthat,withtheexceptionofheating,ventilating,andairconditioning(HVAC)equipment,additionalrequirements(e.g.,ISUISTrequirementsandindustrystandards)existwhichenhancethedevelopmentofsurveillanceprocedures.AllHVACproceduresusedtoperformTechnicalSpecificationsurveillanceswerereviewedtoensuretheintentoftheTechnicalSpecificationsurveillanceweremet.ThisreviewwascompletedonNovember24,1997.4.CORRECTIVESTEPSTOAVOIDFURTHERVIOLATIONSFPLQualityInstruction(QI)QI-S-PSL-1,"Preparation,Revision,Review/ApprovalofProcedures,"Section5.5requiresthatsiteproceduresbeperiodicallyreviewed.ThisQIwasrevisedtorequireaqualifiedindependentreviewofproceduresthataFectsurveillancesorteststoensurethattheprocedureadequatelyimplementstheintentofUpdatedFinalSafetyAnalysisReport(UFSAR)surveillancedescriptionsandTechnicalSpecificationsurveillancerequirementswhenprocedureperiodicreviewsareconducted.ThisrevisionwasapprovedonNovember28,1997.5.FullcompliancewasachievedonOctober13,1997,whentherevisiontoprocedureNOP2-2000020,"ContainmentCoolingSystemOperation,"wasapproved.
 
50-389 St. Lucie Plant, Unit 2, Florida Power
& Light Co.
 
.NAME AUTHOR AFFILIATION LAND1S,K.D.
 
Region 2 (Post 820201)
RECIP.NAME RECIPIENT AFFIL'IDION PLUNKETT,T.F-.
Florida Power
&. Light Co.
 
SUBJECT: Ack receipt of'980102'tr. informing, NRC of steps taken to correct violations noted in insprept 50-335/97-15
&
50-389/97-15 on 971211..
DZSTRZBUTZON, CODE.:
ZE01D COPIES. RECEZVED: LTR. f ENCL 5 SZZE'ITTLE:.
General (50 Dkt):-Insp Rept/Notice of. Violation Response, NOTES;"
DOCKET 05000335 05000389 RECIPIENT.
 
ID CODE/NAME PD2-3 PD'NTERNAL:
ACRS ILE'ENTE PM/PECB NUDOCS-ABSTRACT OGC/HDS3 COPIES-LTTR ENCL
 
11'
 
RECXPIENT XD CODE/NAME WIENS',''.
k AEOD/SPD/RAB DEDRO NRR/DRCH/HHFB
, NRR/DRPM/PERB OE DIR RGN2 FILE
 
COPIES LTTR ENCL
 
1
 
1
.1
 
0 R
Y AL: LITCO BRYCE,J H NRC PDR NOAC NUDOCS FULLTEXT D
 
C E
N
.
NOTE TO ALL nRIDSE RECIPIENTS PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRZBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL
 
==SUBJECT:==
NOTICE-OF VIGLATION '-
(NRC INSPECTION REPORT NO. 50-335/97-15 AND 50-389/97-15)
 
==Dear Mr. Plunkett:==
Thank you for your response'f January 2,
1998, to our Notice of -Violation issued on December 11, 1997,'concerning activities conducted at your St. Lucie facility.
 
We have evaluated your response and found that it meets the requirement of 10 CFR 2.201.
 
We will examine the implementation of your corrective actions during future inspections.
 
We appreciate your cooperation in this matter.
 
Sincere1y, Docket Nos. 50-335, 50-389 License Nos.
 
DPR-67, NPF-16 (original signed by Kerry D. Landis)
J Kerry D. Landis, Chief Reactor Projects Branch 3 Division of Reactor Projects 9802040i44 980i20 PDR ADDCK 05000335
 
PDR
 
FP8L J.
 
A. Stall Site Vice President St. Lucie Nuclear Pl:ant 6351 South Ocean Drive Jensen Beach.
 
FL 34957 H.
 
N-. Paduano, Manager Licensing and Special Programs Florida Power and Light Company P; 0.
 
Box 14000 Juno Beach, FL 33408-0420'.
Scarola Plant General Manager, St. Lucie Nuclear Plant 6351 South Ocean Drive Jensen Beach, FL 34957 E. J.
 
Weinkam Licensing Manager St. Lucie Nuclear Plant 6351 South Ocean Drive Jensen Beach, FL 34957 M. S.
 
Ross, Attorney Florida Power 8 Light P. 0.
 
Box 14000 Juno Beach, FL 33408-0420 John T. Butler, Esq.
 
Steel, Hector and Davis 4000 Southeast Financial Center Miami. FL 33131-2398 Bill Passetti Office of Radiation Control Department of Health and Rehabilitative Services 1317 Winewood Boulevard Tallahassee, FL 32399-0700 Joe Myers, Director Division of Emergency Preparedness Department of Community Affairs 2740 Centerview Drive Tallahassee.
 
FL 32399-2100 Douglas Anderson County Administrator St. Lucie County 2300 Virginia Avenue Ft. Pierce.
 
FL 34982
 
FPEL Distributi on:
L. Wiens, NRR S.
 
Rudisai 1, RII.
 
EA File (B.
 
Summer s.
 
OE)
PUBLIC NRC Resident Inspector
<<
U.S. Nuclear Regulatory Comm.
 
7585 South'Highway A1A Jensen
'Bea'ch.FL 34957-2010 OFFICE SIGNATURE R:DRP DAI COPT?
NO OFFICIAL RECORD CDPT
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'YE NO TES NO TES NO T lUWE:
G:XSTLUCIEXLETTERSMCK9715.LTR
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Latest revision as of 13:16, 8 January 2025

Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Repts 50-335/97-15 & 50-389/97-15
ML17229A597
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 01/20/1998
From: Landis K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Plunkett T
FLORIDA POWER & LIGHT CO.
References
50-335-97-15, 50-389-97-15, EA-97-501, NUDOCS 9802040144
Download: ML17229A597 (4)


Text

CATEGORY 2 v

REGULATORY INFORMATION.DISTRIBUTION SYSTEM (RXDS)

.'CCESSION NBR:9802040144'OC.DATE:.98/01/20>>

NOTARIZED: NO CIL':50'-335; St. Lucie Plant, Unit 1, Flori'da Power.

& Li'ght Co.

50-389 St. Lucie Plant, Unit 2, Florida Power

& Light Co.

.NAME AUTHOR AFFILIATION LAND1S,K.D.

Region 2 (Post 820201)

RECIP.NAME RECIPIENT AFFIL'IDION PLUNKETT,T.F-.

Florida Power

&. Light Co.

SUBJECT: Ack receipt of'980102'tr. informing, NRC of steps taken to correct violations noted in insprept 50-335/97-15

&

50-389/97-15 on 971211..

DZSTRZBUTZON, CODE.:

ZE01D COPIES. RECEZVED: LTR. f ENCL 5 SZZE'ITTLE:.

General (50 Dkt):-Insp Rept/Notice of. Violation Response, NOTES;"

DOCKET 05000335 05000389 RECIPIENT.

ID CODE/NAME PD2-3 PD'NTERNAL:

ACRS ILE'ENTE PM/PECB NUDOCS-ABSTRACT OGC/HDS3 COPIES-LTTR ENCL

11'

RECXPIENT XD CODE/NAME WIENS',.

k AEOD/SPD/RAB DEDRO NRR/DRCH/HHFB

, NRR/DRPM/PERB OE DIR RGN2 FILE

COPIES LTTR ENCL

1

1

.1

0 R

Y AL: LITCO BRYCE,J H NRC PDR NOAC NUDOCS FULLTEXT D

C E

N

.

NOTE TO ALL nRIDSE RECIPIENTS PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRZBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL

SUBJECT:

NOTICE-OF VIGLATION '-

(NRC INSPECTION REPORT NO. 50-335/97-15 AND 50-389/97-15)

Dear Mr. Plunkett:

Thank you for your response'f January 2,

1998, to our Notice of -Violation issued on December 11, 1997,'concerning activities conducted at your St. Lucie facility.

We have evaluated your response and found that it meets the requirement of 10 CFR 2.201.

We will examine the implementation of your corrective actions during future inspections.

We appreciate your cooperation in this matter.

Sincere1y, Docket Nos. 50-335, 50-389 License Nos.

DPR-67, NPF-16 (original signed by Kerry D. Landis)

J Kerry D. Landis, Chief Reactor Projects Branch 3 Division of Reactor Projects 9802040i44 980i20 PDR ADDCK 05000335

PDR

FP8L J.

A. Stall Site Vice President St. Lucie Nuclear Pl:ant 6351 South Ocean Drive Jensen Beach.

FL 34957 H.

N-. Paduano, Manager Licensing and Special Programs Florida Power and Light Company P; 0.

Box 14000 Juno Beach, FL 33408-0420'.

Scarola Plant General Manager, St. Lucie Nuclear Plant 6351 South Ocean Drive Jensen Beach, FL 34957 E. J.

Weinkam Licensing Manager St. Lucie Nuclear Plant 6351 South Ocean Drive Jensen Beach, FL 34957 M. S.

Ross, Attorney Florida Power 8 Light P. 0.

Box 14000 Juno Beach, FL 33408-0420 John T. Butler, Esq.

Steel, Hector and Davis 4000 Southeast Financial Center Miami. FL 33131-2398 Bill Passetti Office of Radiation Control Department of Health and Rehabilitative Services 1317 Winewood Boulevard Tallahassee, FL 32399-0700 Joe Myers, Director Division of Emergency Preparedness Department of Community Affairs 2740 Centerview Drive Tallahassee.

FL 32399-2100 Douglas Anderson County Administrator St. Lucie County 2300 Virginia Avenue Ft. Pierce.

FL 34982

FPEL Distributi on:

L. Wiens, NRR S.

Rudisai 1, RII.

EA File (B.

Summer s.

OE)

PUBLIC NRC Resident Inspector

<<

U.S. Nuclear Regulatory Comm.

7585 South'Highway A1A Jensen

'Bea'ch.FL 34957-2010 OFFICE SIGNATURE R:DRP DAI COPT?

NO OFFICIAL RECORD CDPT

/

/

/

/

'YE NO TES NO TES NO T lUWE:

G:XSTLUCIEXLETTERSMCK9715.LTR

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TES NO

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TES NO