ML17306A730: Difference between revisions

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| number = ML17306A730
| number = ML17306A730
| issue date = 05/14/1992
| issue date = 05/14/1992
| title = Responds to NRC 920407 Ltr Re Violations Noted in Insp Rept 50-528/92-05 on 920126-0229.Corrective Actions:Hydrogen Test Bottles,Filled by Local Vendor,Removed from Svc,Quarantined & Returned to Vendor & Condition Rept Initiated
| title = Responds to NRC Re Violations Noted in Insp Rept 50-528/92-05 on 920126-0229.Corrective Actions:Hydrogen Test Bottles,Filled by Local Vendor,Removed from Svc,Quarantined & Returned to Vendor & Condition Rept Initiated
| author name = CONWAY W F
| author name = Conway W
| author affiliation = ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
| author affiliation = ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
| addressee name =  
| addressee name =  
Line 11: Line 11:
| contact person =  
| contact person =  
| document report number = 102-02147-WFC-T, 102-2147-WFC-T, NUDOCS 9205200206
| document report number = 102-02147-WFC-T, 102-2147-WFC-T, NUDOCS 9205200206
| title reference date = 04-07-1992
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE
| page count = 31
| page count = 31
}}
}}
See also: [[followed by::IR 05000528/1992005]]


=Text=
=Text=
{{#Wiki_filter:ACCELERATED
{{#Wiki_filter:ACCELERATED DISTRIBUTION DEMONSTPA.TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
DISTRIBUTION
ESSION NBR:9205200206 DOC.DATE: 92/05/14 NOTARIZED:
DEMONSTPA.TION
NO
SYSTEM REGULATORY
'OCKET Lij'IL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.
INFORMATION
Arizona Public Service Co.
DISTRIBUTION
(formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SYSTEM (RIDS)ESSION NBR:9205200206
 
DOC.DATE: 92/05/14 NOTARIZED:
==SUBJECT:==
NO'OCKET Lij'IL:STN-50-528
Responds to NRC 920407 ltr re violations noted in Insp Rept 50-528/92-05 on 920126-0229.Corrective actions:hydrogen test bottles, filled by local vendor, removed from svc,quarantined
Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH.NAME AUTHOR AFFILIATION
& returned to vendor
CONWAY,W.F.
& condition rept initiated.
Arizona Public Service Co.(formerly Arizona Nuclear Power RECIP.NAME
DISTRIBUTION CODE IEOID COPIES RECEIVED LTR,L ENCL /
RECIPIENT AFFILIATION
SIZE' TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response D
Document Control Branch (Document Control Desk)SUBJECT: Responds to NRC 920407 ltr re violations
NOTES:STANDARDIZED PLANT 05000528 RECIPIENT ID CODE/NAME PD5 PD THOMPSON,M INTERNAL: ACRS AEOD/DEIIB DEDRO t
noted in Insp Rept 50-528/92-05
NRR/DLPQ/LHFBPT NRR/DOEA/OEAB NRR/DST/DIR 8E2 NUDOCS-ABSTRACT OGC/HDS1 RGN5 FILE 01 EXTERNAL: EG&G/BRYCE,J.H.
on 920126-0229.Corrective
NSIC COPIES LTTR ENCL 1
actions:hydrogen
1 1
test bottles, filled by local vendor, removed from svc,quarantined
1 2
&returned to vendor&condition rept initiated.
2 1
DISTRIBUTION
1 1
CODE IEOID COPIES RECEIVED LTR,L ENCL/SIZE'TITLE: General (50 Dkt)-Insp Rept/Notice
1 1
of Violation Response D NOTES:STANDARDIZED
1 1
PLANT 05000528 RECIPIENT ID CODE/NAME PD5 PD THOMPSON,M
1 1
INTERNAL: ACRS AEOD/DEIIB
1 1
DEDRO t NRR/DLPQ/LHFBPT
1 1
NRR/DOEA/OEAB
1 1
NRR/DST/DIR
1 1
8E2 NUDOCS-ABSTRACT
1 1
OGC/HDS1 RGN5 FILE 01 EXTERNAL: EG&G/BRYCE,J.H.
1 RECIPIENT ID CODE/NAME TRAMMELL,C AEOD AEOD/DSP/TPAB NRR MORISSEAU,D NRR/DLPQ/LPEB10 NRR/DREP/PEPB9H NRR/PMAS/ILRB12 O~
NSIC COPIES LTTR ENCL 1 1 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 RECIPIENT ID CODE/NAME TRAMMELL, C AEOD AEOD/DSP/TPAB
EG FILE 02 NRC PDR COPIES LTTR ENCL 1
NRR MORISSEAU,D
1 1
NRR/DLPQ/LPEB10
1 1
NRR/DREP/PEPB9H
1 1
NRR/PMAS/ILRB12
1 1
O~EG FILE 02 NRC PDR COPIES LTTR ENCL 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 D D R D NOTE TO ALL"RIDS" RECIPIENTS:
1 1
D D P LEASE HELP US TO REDUCE WASTE!CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT.20079)TO ELIMINATE YOUR NAhIE FROM DISTRIBUTION
1 1
LISTS FOR DOCUMENTS YOU DON'T NEED!TAL NUMBER OF COPIES REQUIRED: LTTR 24 ENCL 24  
1 1
1 1
WILLIAM F.CONWAY EXECUTNEVICEPRESLDENT
1 1
NUCLEAR Arizona Public Service Company P.O.BOX 53999~PHOENIX.ARIZONA 85072-3999
1 D
102-02147-WFC/TRB/JRB
D R
May 14, 1992 U.S.Nuclear Regulatory
D NOTE TO ALL"RIDS" RECIPIENTS:
Commission
D D
Attention:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAhIE FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
Document Control Desk Mail Station: P1-37 Washington, DC 20555 Reference:
TAL NUMBER OF COPIES REQUIRED:
Letter dated April 7, 1992, from S.A.Richards, Chief, Reactor Projects Branch, NRC, to W.F.Conway, Executive Vice President, Nuclear, Arizona Public Service Company.Gentlemen:
LTTR 24 ENCL 24
Subject: PALO VERDE NUCLEAR GENERATING
 
STATION (PVNGS)UNITS 1, 2 AND 3 REPLY TO NOTICE OF VIOLATIONS
WILLIAMF. CONWAY EXECUTNEVICEPRESLDENT NUCLEAR Arizona Public Service Company P.O. BOX 53999
50-528/92-05-01, 50-528/92-05-02
~
AND 50-528/92-05;03
PHOENIX. ARIZONA85072-3999 102-02147-WFC/TRB/JRB May 14, 1992 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Mail Station: P1-37 Washington, DC 20555
File: 92-070-026
 
Arizona Public Service Company (APS)has reviewed NRC Inspection
==Reference:==
Report 50-528, 529, 530/92-05 and the Notice of Violations
Letter dated April 7, 1992, from S. A. Richards, Chief, Reactor Projects Branch, NRC, to W. F. Conway, Executive Vice President,
dated April 7, 1992.Pursuant to the provisions
: Nuclear, Arizona Public Service Company.
of 10 CFR 2.201, APS'esponse
Gentlemen:
is attached.Appendix A to this letter is a restatement
 
of the Notice of Violations.
==Subject:==
APS'esponse
PALO VERDE NUCLEAR GENERATING STATION (PVNGS)
is provided in Attachment
UNITS 1, 2 AND 3 REPLY TO NOTICE OF VIOLATIONS50-528/92-05-01, 50-528/92-05-02 AND 50-528/92-05;03 File: 92-070-026 Arizona Public Service Company (APS) has reviewed NRC Inspection Report 50-528, 529, 530/92-05 and the Notice of Violations dated April7, 1992. Pursuant to the provisions of 10 CFR 2.201, APS'esponse is attached.
1.Per telephone conversation
Appendix A to this letter is a restatement of the Notice of Violations. APS'esponse is provided in Attachment 1.
on May 6, 1992, between H.J.Wong, NRC, and T.R.Bradish, APS, an extension of the due date for this response from May 7, 1992, to May 15, 1992.This extension was necessary as a result of PVNGS Unit 3 being in an ALERT emergency classification
Per telephone conversation on May 6, 1992, between H. J. Wong, NRC, and T. R. Bradish, APS, an extension of the due date for this response from May 7, 1992, to May 15, 1992.
from May 4, 1992, through May 6, 1992.Should you have any questions regarding this response, please contact me.Sincerely,'0 WFC/TRB/JRB/dmn
This extension was necessary as a result of PVNGS Unit 3 being in an ALERT emergency classification from May 4, 1992, through May 6, 1992.
Attachments
Should you have any questions regarding this response, please contact me.
1.Appendix A-Restatement
Sincerely,
of Notice of Violations
'0 WFC/TRB/JRB/dmn Attachments 1.
2.Attachment
Appendix A - Restatement of Notice of Violations 2.
1-Reply to Notice of Violations
Attachment 1 - Reply to Notice of Violations cc:
cc: J.B.Martin A i-i C'.nn 9205200206
J. B. Martin A i-i C'.nn 9205200206 920514 PDR ADDCK 05000528 8
920514 PDR ADDCK 05000528 8 PDR p7p,~)stI r Iiq5  
PDR p7p, ~)stI r
'
Iiq5
APPENDIX A RESTATEMENT
 
OF NOTICE OF VIOLATIONS
APPENDIX A RESTATEMENT OF NOTICE OF VIOLATIONS50-528/92-05-02, 50-528/92-05-01 AND 50-528/92-05-03 NRC INSPECTION CONDUCTED JANUARY26, 1992-FEBRUARY 29) 1992 INSPECTION REPORT NOS. 50-528, 529, AND 530/92-05
50-528/92-05-02, 50-528/92-05-01
 
AND 50-528/92-05-03
i
NRC INSPECTION
 
CONDUCTED JANUARY 26, 1992-FEBRUARY 29)1992 INSPECTION
RESTATEMENT OF NOTICE OF VIOLATIONS50-528 92-05-02 50-528 92-0541 AND 50-528 92-05-03 During an NRC inspection conducted on January 26 through February 29, 1992, three violations of NRC requirements were identified.
REPORT NOS.50-528, 529, AND 530/92-05  
In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Action," 10 CFR Part 2, Appendix C, the violations are listed below:
i  
A.
RESTATEMENT
Unit 1 Technical Specification 6.8.1 states, in part, that written procedures shall be established, implemented, and maintained covering the activities recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February, 1978.
OF NOTICE OF VIOLATIONS
Regulatory Guide 1.33, Revision 2, Appendix A, recommends surveillance procedures and general plant operating procedures.
50-528 92-05-02 50-528 92-0541 AND 50-528 92-05-03 During an NRC inspection
Surveillance procedure 36ST-9SB02, "PPS Bistable Trip Units Functional Test," Step 8.11.6.2, requires the test performer to "ensure LO SG2 PRESS Trip Setpoint (Parameter
conducted on January 26 through February 29, 1992, three violations
: 12) is at the MAXIMUMVALUEwhen in Mode 1 or
of NRC requirements
: 2. Adjust as necessary."
were identified.
Contrary to the above, on February 4, 1992, when performing step 8.11.6.2, the test performer failed to ensure the LO SG2 PRESS trip setpoint (parameter
In accordance
: 12) was at the maximum value when the unit was in Mode 1, resulting in the setpoint being approximately 50 pounds per square inch less that [sic] the minimum value allowed by Technical Specifications 2.2.1 and 3.3.2.
with the"General Statement of Policy and Procedure for NRC Enforcement
2.
Action," 10 CFR Part 2, Appendix C, the violations
General operating procedure 40DP-90P05, "Control Room Data Sheet Instructions,
are listed below: A.Unit 1 Technical Specification
" Step 2.3.2, requires that a reactor operator report "any abnormal and/or unusual condition" while fillingout the Control Room Data Sheets.
6.8.1 states, in part, that written procedures
Contrary to the above, on February 4, 1992, at 5:00 pm, while fillingout the Control Room Data Sheets, the reactor operator failed to note that the 42 steam generator low pressure setpoint was incorrectly set.
shall be established, implemented, and maintained
This is a Severity Level IV Violation (Supplement I) applicable to Unit 1.
covering the activities
B.
recommended
Unit 1 Technical Specification 6.8.1 states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix Aof Regulatory Guide 1.33, Revision 2, February 1978.
in Appendix A of Regulatory
Page 1
Guide 1.33, Revision 2, February, 1978.Regulatory
 
Guide 1.33, Revision 2, Appendix A, recommends
Regulatory Guide 1.33, Appendix A; recommends procedures for performing maintenance and states that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.
surveillance
Licensee Procedure 36MT-9RI06, 'VNhdrawal of ICICables," Section 8.4.5, requires the control element assembly (CEA) hoist to be used when withdrawing fixed incore instruments (ICls) for refueling operations.
procedures
Contrary to the above, on February 25, 1992, the licensee failed to implement Procedure 36MT-9RI06, in that fixed ICI455 was manually withdrawn without using the CEA hoist.
and general plant operating procedures.
This is a Severity Level IV violation (Supplement I) applicable to Unit 1.
Surveillance
C.
procedure 36ST-9SB02,"PPS Bistable Trip Units Functional
10 CFR 50, Appendix B, Criterion XII, requires that measures be established to assure that tools, gages, instruments, and other measuring and testing devices used in activities affecting quality are properly controlled, calibrated, and adjusted at specified periods to maintain accuracy within necessary limits.
Test," Step 8.11.6.2, requires the test performer to"ensure LO SG2 PRESS Trip Setpoint (Parameter
Contrary to the above, no measures were established to assure that calibration gas used for performance of containment hydrogen monitor surveillance tests, an activity affecting quality, was properly controlled and calibrated.
12)is at the MAXIMUM VALUE when in Mode 1 or 2.Adjust as necessary." Contrary to the above, on February 4, 1992, when performing
Specifically, on February 11,
step 8.11.6.2, the test performer failed to ensure the LO SG2 PRESS trip setpoint (parameter
: 1992, the Unit 2 Containment Hydrogen Monitor Channel A
12)was at the maximum value when the unit was in Mode 1, resulting in the setpoint being approximately
surveillance test (Procedure 36ST-9HP03) was performed using a calibration gas that was not procured from a QA approved vendor and no other QA controls were provided to assure the proper calibration of the gas.
50 pounds per square inch less that[sic]the minimum value allowed by Technical Specifications
On February 13, 1992, one containment hydrogen monitor each in Units 1 and 3, were also determined to have had surveillance tests performed with calibration gas that was not properly controlled or calibrated.
2.2.1 and 3.3.2.2.General operating procedure 40DP-90P05,"Control Room Data Sheet Instructions," Step 2.3.2, requires that a reactor operator report"any abnormal and/or unusual condition" while filling out the Control Room Data Sheets.Contrary to the above, on February 4, 1992, at 5:00 pm, while filling out the Control Room Data Sheets, the reactor operator failed to note that the 42 steam generator low pressure setpoint was incorrectly
set.This is a Severity Level IV Violation (Supplement
I)applicable
to Unit 1.B.Unit 1 Technical Specification
6.8.1 states, in part, that written procedures
shall be established, implemented, and maintained
covering the applicable
procedures
recommended
in Appendix A of Regulatory
Guide 1.33, Revision 2, February 1978.Page 1  
Regulatory
Guide 1.33, Appendix A;recommends
procedures
for performing
maintenance
and states that maintenance
that can affect the performance
of safety-related
equipment should be properly preplanned
and performed in accordance
with written procedures, documented
instructions, or drawings appropriate
to the circumstances.
Licensee Procedure 36MT-9RI06,'VNhdrawal
of ICI Cables," Section 8.4.5, requires the control element assembly (CEA)hoist to be used when withdrawing
fixed incore instruments (ICls)for refueling operations.
Contrary to the above, on February 25, 1992, the licensee failed to implement Procedure 36MT-9RI06, in that fixed ICI 455 was manually withdrawn without using the CEA hoist.This is a Severity Level IV violation (Supplement
I)applicable
to Unit 1.C.10 CFR 50, Appendix B, Criterion XII, requires that measures be established
to assure that tools, gages, instruments, and other measuring and testing devices used in activities
affecting quality are properly controlled, calibrated, and adjusted at specified periods to maintain accuracy within necessary limits.Contrary to the above, no measures were established
to assure that calibration
gas used for performance
of containment
hydrogen monitor surveillance
tests, an activity affecting quality, was properly controlled
and calibrated.
Specifically, on February 11, 1992, the Unit 2 Containment
Hydrogen Monitor Channel A surveillance
test (Procedure
36ST-9HP03)
was performed using a calibration
gas that was not procured from a QA approved vendor and no other QA controls were provided to assure the proper calibration
of the gas.On February 13, 1992, one containment
hydrogen monitor each in Units 1 and 3, were also determined
to have had surveillance
tests performed with calibration
gas that was not properly controlled
or calibrated.
This is a Severity Level IV violation (Supplement
This is a Severity Level IV violation (Supplement
1)applicable
: 1) applicable to Units 1, 2 and 3.
to Units 1, 2 and 3.Page 2  
Page 2
 
ATTACHMENT
ATTACHMENT1 REPLY TO NOTICE OF VIOLATIONS 50-528/92-05-02, 50-528/92-05-0 t AND 50-528/92-05-03 NRC INSPECTION CONDUCTED JANUARY26, 1992-FEBRUARY 29, 1992 INSPECTION REPORT NOS. 50-528, 529, 530/92-05
1 REPLY TO NOTICE OF VIOLATIONS
 
50-528/92-05-02, 50-528/92-05-0
0 REPLY TO NOTICE OF VIOLATION50-528 92-05-02 Reason For The Violation The reason for both examples of the violation was a cognitive personnel error.
t AND 50-528/92-05-03
During scheduled surveillance testing of the Unit 1, number 1 steam generator low steam generator pressure trip setpoint on February 4, 1992, the RPS/ESFAS channel
NRC INSPECTION
'B'ow steam generator pressure trips for both the number 1 and number 2 steam generators were placed in bypass, as required by 36ST-9SB02, "PPS Bistable Trip Units Functional Test."
CONDUCTED JANUARY 26, 1992-FEBRUARY 29, 1992 INSPECTION
During this surveillance, the low steam generator pressure setpoint reset button was depressed, as required, resulting in the channel 'B'ow steam generator pressure trip setpoint for both steam generators being reduced to approximately 200 psia e
REPORT NOS.50-528, 529, 530/92-05  
below the actual steam generator pressures.
The surveillance test subsequently requires resetting of the channel 'B'ow steam generator pressure trip setpoint to verify proper operation.
0 REPLY TO NOTICE OF VIOLATION 50-528 92-05-02 Reason For The Violation The reason for both examples of the violation was a cognitive personnel error.During scheduled surveillance
The channel 'B'ow steam generator pressure trip setpoint for the number 1
testing of the Unit 1, number 1 steam generator low steam generator pressure trip setpoint on February 4, 1992, the RPS/ESFAS channel'B'ow steam generator pressure trips for both the number 1 and number 2 steam generators
steam generator was reset in accordance with the surveillance test procedure.
were placed in bypass, as required by 36ST-9SB02,"PPS Bistable Trip Units Functional
While checking the channel 'B'ow steam generator pressure trip setpoint for the number 2 steam generator, the maintenance I&Ctechnician performing the surveillance test did not select the number 2 steam generator low steam generator pressure setpoint on the select switch. This resulted in the maintenance l&Ctechnician erroneously using the previously verified number 1 steam generator channel 'B'ow steam generator pressure trip setpoint to check the numbers 2 steam generator channel 'B'ow steam generator pressure trip setpoint.
Test." During this surveillance, the low steam generator pressure setpoint reset button was depressed, as required, resulting in the channel'B'ow steam generator pressure trip setpoint for both steam generators
The RPS/ESFAS channel '8'ow steam generator Page 1 of 11
being reduced to approximately
 
200 psia e below the actual steam generator pressures.
pressure trips for both the number 1 and number 2 steam generators were taken out of bypass following completion of the applicable portion of the surveillance test.
The surveillance
N Approximately'one-half hour after the channel 'B'ow steam generator pressure trips were taken out of bypass, a Unit 1 control room reactor operator checked the low steam generator pressure trip setpoints as part of a scheduled setpoint check.
test subsequently
The operations procedure for control room data sheets (40DP-9OP05, "Control Room Data Sheet Instructions" ) requires any abnormal and/or unusual conditions or readings be reported to the Shift Supervisor or Assistant Shift Supervisor.
requires resetting of the channel'B'ow steam generator pressure trip setpoint to verify proper operation.
The control room reactor operator did not identify that the RPS/ESFAS channel 'B'ow steam generator pressure trip setpoint forthe number 2 steam generator was below the minimum allowed Technical Specification value, as required.
The channel'B'ow steam generator pressure trip setpoint for the number 1 steam generator was reset in accordance
Corrective Ste s That Have Been Taken And The Results Achieved Approximately one hour after the control room reactor operator failed to identify the incorrect RPS/ESFAS channel 'B'ow steam generator pressure trip setpoint for the Unit 1, number 2 steam generator, the Assistant Shift Supervisor discovered that the setpoint was below the minimum allowed Technical Specification value. The channel
with the surveillance
'B'ow steam generator pressure trip for the number 2 steam generator was declared inoperable and the Unit 1 maintenance l&C department was notified.
test procedure.
The low steam generator pressure trip setpoint was reset to the required value approximately one hour later.
While checking the channel'B'ow steam generator pressure trip setpoint for the number 2 steam generator, the maintenance
Page 2 of 11
I&C technician
 
performing
A Condition Report/Disposition Request was initiated to conduct an investigation of this event and subsequently determined the cause to be personnel error.
the surveillance
The involved control room reactor operator and maintenance I8 C technician have been disciplined in accordance with the APS Positive Discipline Program.
test did not select the number 2 steam generator low steam generator pressure setpoint on the select switch.This resulted in the maintenance
A control room night order discussing this event was issued in Units 1, 2, and 3 to reinforce the importance of attention to detail in performing routine checks thoroughly.
l&C technician
Briefings have been conducted on this event with Units 1, 2, and 3 maintenance l&C technicians.
erroneously
As an enhancement, the surveillance test procedure (36ST-9SB02) has been revised to add detailed action steps to direct performers on how to attain and determine the low steam generator pressure trip setpoints for added assurance that the minimum e
using the previously
allowed value for the trip setpoint is attained prior to removing the low steam generator pressure trip from bypass.
verified number 1 steam generator channel'B'ow steam generator pressure trip setpoint to check the numbers 2 steam generator channel'B'ow steam generator pressure trip setpoint.The RPS/ESFAS channel'8'ow steam generator Page 1 of 11  
The investigation results were provided to the NRC in a letter from James M.
Levine dated March 5, 1992 (Licensee Event Report 528/92-003-00).
pressure trips for both the number 1 and number 2 steam generators
Corrective Ste s That Will Be Taken To Avoid Further Violations The corrective actions discussed above are considered adequate to avoid further violations and no additional corrective actions are planned.
were taken out of bypass following completion
Page 3of11
of the applicable
 
portion of the surveillance
~
test.N Approximately'one-half
 
hour after the channel'B'ow steam generator pressure trips were taken out of bypass, a Unit 1 control room reactor operator checked the low steam generator pressure trip setpoints as part of a scheduled setpoint check.The operations
Date When Full Com Ilance Will Be Achieved Full compliance was achieved on February 4, 1992, upon restoring the Unit 1, steam generator number 2 low steam generator pressure trip setpoint.to the minimum allowed Technical Specification value.
procedure for control room data sheets (40DP-9OP05,"Control Room Data Sheet Instructions")requires any abnormal and/or unusual conditions
Additional Information The inspection report cover letter requests an assessment of the need for independent verification of the reactor trip setpoints adjusted during surveillance testing.
or readings be reported to the Shift Supervisor
During the investigation of this event, APS evaluated the need for independent verification of as-left reactor trip setpoints.
or Assistant Shift Supervisor.
Although no previous examples of improper restoration of reactor trip setpoints at the conclusion of surveillance testing were identified, APS e
The control room reactor operator did not identify that the RPS/ESFAS channel'B'ow steam generator pressure trip setpoint for the number 2 steam generator was below the minimum allowed Technical Specification
concluded that an additional check of as-left reactor trip setpoints would be prudent, if the setpoint was. adjusted outside the acceptance criteria during the surveillance test.
value, as required.Corrective
Surveillance testing meeting this criteria was identified for the low steam generator pressure trip and the low pressurizer pressure trip.
Ste s That Have Been Taken And The Results Achieved Approximately
Changes to the PPS bistable trip units functional test procedure (36ST-9SB02) have been initiated to require a separate check to verifythat the low steam generator pressure trip setpoint and the low pressurizer pressure trip setpoint are within their acceptance criteria prior to removing the trips from bypass.
one hour after the control room reactor operator failed to identify the incorrect RPS/ESFAS channel'B'ow steam generator pressure trip setpoint for the Unit 1, number 2 steam generator, the Assistant Shift Supervisor
These changes will be implemented by June 30, 1992.
discovered
Page 4 of 11
that the setpoint was below the minimum allowed Technical Specification
 
value.The channel'B'ow steam generator pressure trip for the number 2 steam generator was declared inoperable
REPLY TO NOTICE OF VIOLATION50-528 92-05-01 Reason For The Violation The reason for the violation was an improper procedural step and subsequent implementation of the flexibilityallowed by the step.
and the Unit 1 maintenance
Prior to February 25, 1992, during Unit 1 refueling activities, sixty incore instruments
l&C department
,(ICIs) had been withdrawn in accordance with maintenance procedure 36MT-9RI06, "Withdrawal OfThe Incore Instruments For Reactor Refueling Operations," leaving one ICI installed. On February 25, 1992, scaffolding had been erected at the entrance to the east end of the refueling canal.
was notified.The low steam generator pressure trip setpoint was reset to the required value approximately
This scaffolding prevented placement of the control element assembly (CEA)/ICI change platform above the ICI holding frame, and consequently the use of the CEA hoist to withdraw the final ICI, as required by 36MT-9RI06, Step 8.4.5. The a
one hour later.Page 2 of 11  
involved Work Group Supervisor reviewed 36MT-9RI06 for an alternate means to remove the final ICI. Step 7.7 of 36MT-9RI06 states, 'This procedure should be considered a
guideline, the I&C technician and Work Group Supervisor should have flexibilityin the order of work performance and should decide the need for some steps depending upon inspection results, such as cleaning of slip tubes, spacers, etc. ".
A Condition Report/Disposition
The Work Group Supervisor interpreted this step as allowing a manual withdrawal of an ICI, in lieu of using the CEA hoist, as required by 36MT-9RI06, Step 8.4.5.
Request was initiated to conduct an investigation
Following the decision to attempt a manual withdrawal of the final ICI, a tailboard meeting was conducted, at which the ICI task shift lead was cautioned on the slow lift requirement and the 500 pound maximum pull requirement of 36MT-9RI06. The radiation Page 5 of 11
of this event and subsequently
 
determined
0 protection department was notified of the planned ICI manual withdrawal.
the cause to be personnel error.The involved control room reactor operator and maintenance
. During the actual ICI withdrawal, a rope was attached to the ICI lift bail and used by a technician on the 140 foot elevation platform to withdraw the ICI.
I8 C technician
A second technician, in the accompaniment of a radiation protection technician, was located in the refuel cavity to wipe the cable as it was withdrawn.
have been disciplined
When the withdrawal was first attempted, the force was greater than anticipated, so the technicians stopped the withdrawal attempt to investigate the cause.
in accordance
A piece of duct tape was removed from the ICI cable and the ICI was successfully withdrawn and secured in the ICI holding frame The duct tape had been left following a preceding, unrelated maintenance activity to replace the ICI seal housing.
with the APS Positive Discipline
Corrective Ste s That Have Been Taken And The Results Achieved A Condition Report/Disposition Request was initiated to investigate this activity and determined the cause discussed above.
Program.A control room night order discussing
The B&W Nuclear Services personnel were briefed on the incident and the need for verbatim procedural compliance was emphasized.
this event was issued in Units 1, 2, and 3 to reinforce the importance
Changes have been made to maintenance procedure 36MT-BRI06, 'Withdrawal Of The Incore Instruments For Reactor Refueling Operations," to delete the phrase, "this procedure should be considered a guideline," from Step 7.7 (Step renumbered as 2.1.2.7) and to revise Step 8.4,5 (Step renumbered as 4.4.12) to allow lifting ICls manually.
of attention to detail in performing
Page 6 of 11
routine checks thoroughly.
 
Briefings have been conducted on this event with Units 1, 2, and 3 maintenance
0 Corrective Ste s That Will Be Taken To Avoid Further Violations The corrective actions discussed above are considered adequate to avoid further violations and no additional corrective actions are planned.
l&C technicians.
Date When Full Com Ilance Will Be Achieved Full compliance was achieved on February 25, 1992, upon completion of the manual withdrawal of the final Unit 1 ICI.
As an enhancement, the surveillance
Page 7 of 11
test procedure (36ST-9SB02)
 
has been revised to add detailed action steps to direct performers
REPLY TO NOTICE OF VIOLATION50-528 92-05-03 Reason For The Violation The reason for the violation was inadequate interim corrective measures upon identification of a quality deficiency.
on how to attain and determine the low steam generator pressure trip setpoints for added assurance that the minimum e allowed value for the trip setpoint is attained prior to removing the low steam generator pressure trip from bypass.The investigation
Aquality deficiency report was initiated in April, 1991, to document that surveillance test procedure 36ST-9HP03, "Containment Hydrogen Monitoring System Calibration Test, Channel A," was inadequate in that the test gas used was not traceable to a calibration standard.
results were provided to the NRC in a letter from James M.Levine dated March 5, 1992 (Licensee Event Report 528/92-003-00).
An action plan was developed to address this deficiency which included actions to establish technical specification and quality requirements for the test gas and locate an acceptable vendor. The test gas used in this surveillance was being purchased on a non-quality related purchase order used to purchase miscellaneous gases, without identifying specific plant applications for each gas.
Corrective
\\
Ste s That Will Be Taken To Avoid Further Violations
Prior to an acceptable vendor being approved, interim measures were taken to ensure the quality of the test gas used in the performance of 36ST-9HP03. A prospective vendor (Air Products and Chemical) was selected based on their use by another Region V utilityas a supplier of safety-related calibration gases.
The corrective
The prospective vendor's quality assurance manual was reviewed and APS concluded that the vendor had adequate processes for ensuring that the required calibration standards are accurately represented in their Certificates of Analysis (CQA). APS also verified that the test gas being supplied by a local vendor was, in fact, being filled by Air Products and Chemical.
actions discussed above are considered
Surveillance test procedures, 36ST-9HP03 and 36ST-9HP04 (Containment Hydrogen Monitoring Page 8of11
adequate to avoid further violations
 
and no additional
System Calibration Test, Channel B) were revised to require the serial number on the test gas bottle to be recorded during performance of the hydrogen monitoring system
corrective
'urveillance test to provide traceability of the gas bottle.
actions are planned.Page 3of11  
Following identification of the critical design attributes that are essential to the dedication process of test gas, APS performed a commercial grade survey of AirProducts and Chemical and identified some minor programmatic issues, none of which would question the accuracy of the hydrogen concentration.
~  
A randomly selected bottle of test gas filled by this vendor which had been supplied to APS was verified to contain the correct hydrogen concentration during this survey.
Date When Full Com Ilance Will Be Achieved Full compliance
On January 9, 1992, due to an urgent need for hydrogen test gas, the system engineer and the Unit 1 l&Cmaintenance department authorized a purchase of hydrogen e
was achieved on February 4, 1992, upon restoring the Unit 1, steam generator number 2 low steam generator pressure trip setpoint.to
test gas filled by a local vendor using the existing non-quality related purchase order. No test gas was in stock at APS and approximately two weeks would have been necessary to obtain the test gas from Air Products and Chemical.
the minimum allowed Technical Specification
Test gas was obtained from the local vendor and used in Unit 1. Although use of hydrogen test gas filled by the local vendor in a hydrogen monitoring system surveillance test was inappropriate, involved personnel did comply with interim corrective measures.
value.Additional
During the week of February 10, 1992, an NRC inspector was observing the hydrogen monitoring system surveillance test on a Unit 2 hydrogen analyzer and noted that the test gas being used was not traceable to the vendor being evaluated for acceptance by APS.
Information
Based on this observation, all three units were checked for hydrogen test gas bottles which were not traceable to the vendor being evaluated for acceptance.
The inspection
Three additional test gas bottles were found, Page 9 of 11
report cover letter requests an assessment
 
of the need for independent
verification
of the reactor trip setpoints adjusted during surveillance
testing.During the investigation
of this event, APS evaluated the need for independent
verification
of as-left reactor trip setpoints.
Although no previous examples of improper restoration
of reactor trip setpoints at the conclusion
of surveillance
testing were identified, APS e concluded that an additional
check of as-left reactor trip setpoints would be prudent, if the setpoint was.adjusted outside the acceptance
criteria during the surveillance
test.Surveillance
testing meeting this criteria was identified
for the low steam generator pressure trip and the low pressurizer
pressure trip.Changes to the PPS bistable trip units functional
test procedure (36ST-9SB02)
have been initiated to require a separate check to verify that the low steam generator pressure trip setpoint and the low pressurizer
pressure trip setpoint are within their acceptance
criteria prior to removing the trips from bypass.These changes will be implemented
by June 30, 1992.Page 4 of 11  
REPLY TO NOTICE OF VIOLATION 50-528 92-05-01 Reason For The Violation The reason for the violation was an improper procedural
step and subsequent
implementation
of the flexibility
allowed by the step.Prior to February 25, 1992, during Unit 1 refueling activities, sixty incore instruments
,(ICIs)had been withdrawn in accordance
with maintenance
procedure 36MT-9RI06,"Withdrawal
Of The Incore Instruments
For Reactor Refueling Operations," leaving one ICI installed.
On February 25, 1992, scaffolding
had been erected at the entrance to the east end of the refueling canal.This scaffolding
prevented placement of the control element assembly (CEA)/ICI change platform above the ICI holding frame, and consequently
the use of the CEA hoist to withdraw the final ICI, as required by 36MT-9RI06, Step 8.4.5.The a involved Work Group Supervisor
reviewed 36MT-9RI06
for an alternate means to remove the final ICI.Step 7.7 of 36MT-9RI06
states,'This procedure should be considered
a guideline, the I&C technician
and Work Group Supervisor
should have flexibility
in the order of work performance
and should decide the need for some steps depending upon inspection
results, such as cleaning of slip tubes, spacers, etc.".The Work Group Supervisor
interpreted
this step as allowing a manual withdrawal
of an ICI, in lieu of using the CEA hoist, as required by 36MT-9RI06, Step 8.4.5.Following the decision to attempt a manual withdrawal
of the final ICI, a tailboard meeting was conducted, at which the ICI task shift lead was cautioned on the slow lift requirement
and the 500 pound maximum pull requirement
of 36MT-9RI06.
The radiationPage 5 of 11  
0 protection
department
was notified of the planned ICI manual withdrawal.
.During the actual ICI withdrawal, a rope was attached to the ICI lift bail and used by a technician
on the 140 foot elevation platform to withdraw the ICI.A second technician, in the accompaniment
of a radiation protection
technician, was located in the refuel cavity to wipe the cable as it was withdrawn.
When the withdrawal
was first attempted, the force was greater than anticipated, so the technicians
stopped the withdrawal
attempt to investigate
the cause.A piece of duct tape was removed from the ICI cable and the ICI was successfully
withdrawn and secured in the ICI holding frame The duct tape had been left following a preceding, unrelated maintenance
activity to replace the ICI seal housing.Corrective
Ste s That Have Been Taken And The Results Achieved A Condition Report/Disposition
Request was initiated to investigate
this activity and determined
the cause discussed above.The B&W Nuclear Services personnel were briefed on the incident and the need for verbatim procedural
compliance
was emphasized.
Changes have been made to maintenance
procedure 36MT-BRI06,'Withdrawal
Of The Incore Instruments
For Reactor Refueling Operations," to delete the phrase,"this procedure should be considered
a guideline," from Step 7.7 (Step renumbered
as 2.1.2.7)and to revise Step 8.4,5 (Step renumbered
as 4.4.12)to allow lifting ICls manually.Page 6 of 11  
0 Corrective
Ste s That Will Be Taken To Avoid Further Violations
The corrective
actions discussed above are considered
adequate to avoid further violations
and no additional
corrective
actions are planned.Date When Full Com Ilance Will Be Achieved Full compliance
was achieved on February 25, 1992, upon completion
of the manual withdrawal
of the final Unit 1 ICI.Page 7 of 11  
REPLY TO NOTICE OF VIOLATION 50-528 92-05-03 Reason For The Violation The reason for the violation was inadequate
interim corrective
measures upon identification
of a quality deficiency.
A quality deficiency
report was initiated in April, 1991, to document that surveillance
test procedure 36ST-9HP03,"Containment
Hydrogen Monitoring
System Calibration
Test, Channel A," was inadequate
in that the test gas used was not traceable to a calibration
standard.An action plan was developed to address this deficiency
which included actions to establish technical specification
and quality requirements
for the test gas and locate an acceptable
vendor.The test gas used in this surveillance
was being purchased on a non-quality
related purchase order used to purchase miscellaneous
gases, without identifying
specific plant applications
for each gas.\Prior to an acceptable
vendor being approved, interim measures were taken to ensure the quality of the test gas used in the performance
of 36ST-9HP03.
A prospective
vendor (Air Products and Chemical)was selected based on their use by another Region V utility as a supplier of safety-related
calibration
gases.The prospective
vendor's quality assurance manual was reviewed and APS concluded that the vendor had adequate processes for ensuring that the required calibration
standards are accurately
represented
in their Certificates
of Analysis (CQA).APS also verified that the test gas being supplied by a local vendor was, in fact, being filled by Air Products and Chemical.Surveillance
test procedures, 36ST-9HP03
and 36ST-9HP04 (Containment
Hydrogen Monitoring
Page 8of11  
System Calibration
Test, Channel B)were revised to require the serial number on the test gas bottle to be recorded during performance
of the hydrogen monitoring
system'urveillance
test to provide traceability
of the gas bottle.Following identification
of the critical design attributes
that are essential to the dedication
process of test gas, APS performed a commercial
grade survey of Air Products and Chemical and identified
some minor programmatic
issues, none of which would question the accuracy of the hydrogen concentration.
A randomly selected bottle of test gas filled by this vendor which had been supplied to APS was verified to contain the correct hydrogen concentration
during this survey.On January 9, 1992, due to an urgent need for hydrogen test gas, the system engineer and the Unit 1 l&C maintenance
department
authorized
a purchase of hydrogen e test gas filled by a local vendor using the existing non-quality
related purchase order.No test gas was in stock at APS and approximately
two weeks would have been necessary to obtain the test gas from Air Products and Chemical.Test gas was obtained from the local vendor and used in Unit 1.Although use of hydrogen test gas filled by the local vendor in a hydrogen monitoring
system surveillance
test was inappropriate, involved personnel did comply with interim corrective
measures.During the week of February 10, 1992, an NRC inspector was observing the hydrogen monitoring
system surveillance
test on a Unit 2 hydrogen analyzer and noted that the test gas being used was not traceable to the vendor being evaluated for acceptance
by APS.Based on this observation, all three units were checked for hydrogen test gas bottles which were not traceable to the vendor being evaluated for acceptance.
Three additional
test gas bottles were found, Page 9 of 11  
which were not traceable to the vendor being evaluated for acceptance.
which were not traceable to the vendor being evaluated for acceptance.
These bottles had been purchased under the non-quality
These bottles had been purchased under the non-quality related purchase order for miscellaneous gases and filled by a local vendor at various times.
related purchase order for miscellaneous
Corrective Ste s That Have Been Taken and Results Achieved Hydrogen test gas bottles which were filled by the local vendor were removed from service, quarantined, and subsequently returned to the vendor.
gases and filled by a local vendor at various times.Corrective
Hydrogen monitoring system surveillance tests were performed on the hydrogen analyzers which had been tested using test gas bottles filled by the local vendor using test gas bottles filled by Air Products and Chemical.
Ste s That Have Been Taken and Results Achieved Hydrogen test gas bottles which were filled by the local vendor were removed from service, quarantined, and subsequently
The tests required no adjustments to hydrogen analyzers, thus validating the tests performed using test gas bottles filled by H
returned to the vendor.Hydrogen monitoring
the local vendor.
system surveillance
AirProducts and Chemical has been accepted by APS as capable of providing test gases of the required'quality and placed on the Commercial Grade Approved Vendor's List.
tests were performed on the hydrogen analyzers which had been tested using test gas bottles filled by the local vendor using test gas bottles filled by Air Products and Chemical.The tests required no adjustments
A quality related purchase order has been issued to Air Products and Chemical to establish a new stock level of test gases.
to hydrogen analyzers, thus validating
The procurement/warehouse tracking (class and item) numbers for test gas have been input into the Materials Management Information System and Station Information Management System for inclusion in corrective maintenance and surveillance test work order packages associated with'hydrogen analyzers.
the tests performed using test gas bottles filled by H the local vendor.Air Products and Chemical has been accepted by APS as capable of providing test gases of the required'quality
Page 10 of 11
and placed on the Commercial
 
Grade Approved Vendor's List.A quality related purchase order has been issued to Air Products and Chemical to establish a new stock level of test gases.The procurement/warehouse
r
tracking (class and item)numbers for test gas have been input into the Materials Management
 
Information
Corrective S e s That Will Be Taken To Avoid Further Violations The corrective actions discussed above are considered adequate to avoid further violations and no additional corrective actions are planned.
System and Station Information
Date When Full Com liance Will Be Achieve Full compliance was achieved on February 14, 1992, upon replacement of the identified test gas bottles which had been filled by the local vendor with test gas bottles filled by Air Products and Chemical.
Management
Page 11 of,11}}
System for inclusion in corrective
maintenance
and surveillance
test work order packages associated
with'hydrogen
analyzers.
Page 10 of 11  
r-
Corrective
S e s That Will Be Taken To Avoid Further Violations
The corrective
actions discussed above are considered
adequate to avoid further violations
and no additional
corrective
actions are planned.Date When Full Com liance Will Be Achieve Full compliance
was achieved on February 14, 1992, upon replacement
of the identified
test gas bottles which had been filled by the local vendor with test gas bottles filled by Air Products and Chemical.Page 11 of,11
}}

Latest revision as of 01:43, 8 January 2025

Responds to NRC Re Violations Noted in Insp Rept 50-528/92-05 on 920126-0229.Corrective Actions:Hydrogen Test Bottles,Filled by Local Vendor,Removed from Svc,Quarantined & Returned to Vendor & Condition Rept Initiated
ML17306A730
Person / Time
Site: Palo Verde Arizona Public Service icon.png
Issue date: 05/14/1992
From: Conway W
ARIZONA PUBLIC SERVICE CO. (FORMERLY ARIZONA NUCLEAR
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
102-02147-WFC-T, 102-2147-WFC-T, NUDOCS 9205200206
Download: ML17306A730 (31)


Text

ACCELERATED DISTRIBUTION DEMONSTPA.TION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ESSION NBR:9205200206 DOC.DATE: 92/05/14 NOTARIZED:

NO

'OCKET Lij'IL:STN-50-528 Palo Verde Nuclear Station, Unit 1, Arizona Publi 05000528 AUTH.NAME AUTHOR AFFILIATION CONWAY,W.F.

Arizona Public Service Co.

(formerly Arizona Nuclear Power RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Responds to NRC 920407 ltr re violations noted in Insp Rept 50-528/92-05 on 920126-0229.Corrective actions:hydrogen test bottles, filled by local vendor, removed from svc,quarantined

& returned to vendor

& condition rept initiated.

DISTRIBUTION CODE IEOID COPIES RECEIVED LTR,L ENCL /

SIZE' TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response D

NOTES:STANDARDIZED PLANT 05000528 RECIPIENT ID CODE/NAME PD5 PD THOMPSON,M INTERNAL: ACRS AEOD/DEIIB DEDRO t

NRR/DLPQ/LHFBPT NRR/DOEA/OEAB NRR/DST/DIR 8E2 NUDOCS-ABSTRACT OGC/HDS1 RGN5 FILE 01 EXTERNAL: EG&G/BRYCE,J.H.

NSIC COPIES LTTR ENCL 1

1 1

1 2

2 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 RECIPIENT ID CODE/NAME TRAMMELL,C AEOD AEOD/DSP/TPAB NRR MORISSEAU,D NRR/DLPQ/LPEB10 NRR/DREP/PEPB9H NRR/PMAS/ILRB12 O~

EG FILE 02 NRC PDR COPIES LTTR ENCL 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 1

1 D

D R

D NOTE TO ALL"RIDS" RECIPIENTS:

D D

PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAhIE FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TAL NUMBER OF COPIES REQUIRED:

LTTR 24 ENCL 24

WILLIAMF. CONWAY EXECUTNEVICEPRESLDENT NUCLEAR Arizona Public Service Company P.O. BOX 53999

~

PHOENIX. ARIZONA85072-3999 102-02147-WFC/TRB/JRB May 14, 1992 U. S. Nuclear Regulatory Commission Attention: Document Control Desk Mail Station: P1-37 Washington, DC 20555

Reference:

Letter dated April 7, 1992, from S. A. Richards, Chief, Reactor Projects Branch, NRC, to W. F. Conway, Executive Vice President,

Nuclear, Arizona Public Service Company.

Gentlemen:

Subject:

PALO VERDE NUCLEAR GENERATING STATION (PVNGS)

UNITS 1, 2 AND 3 REPLY TO NOTICE OF VIOLATIONS50-528/92-05-01, 50-528/92-05-02 AND 50-528/92-05;03 File: 92-070-026 Arizona Public Service Company (APS) has reviewed NRC Inspection Report 50-528, 529, 530/92-05 and the Notice of Violations dated April7, 1992. Pursuant to the provisions of 10 CFR 2.201, APS'esponse is attached.

Appendix A to this letter is a restatement of the Notice of Violations. APS'esponse is provided in Attachment 1.

Per telephone conversation on May 6, 1992, between H. J. Wong, NRC, and T. R. Bradish, APS, an extension of the due date for this response from May 7, 1992, to May 15, 1992.

This extension was necessary as a result of PVNGS Unit 3 being in an ALERT emergency classification from May 4, 1992, through May 6, 1992.

Should you have any questions regarding this response, please contact me.

Sincerely,

'0 WFC/TRB/JRB/dmn Attachments 1.

Appendix A - Restatement of Notice of Violations 2.

Attachment 1 - Reply to Notice of Violations cc:

J. B. Martin A i-i C'.nn 9205200206 920514 PDR ADDCK 05000528 8

PDR p7p, ~)stI r

Iiq5

APPENDIX A RESTATEMENT OF NOTICE OF VIOLATIONS50-528/92-05-02, 50-528/92-05-01 AND 50-528/92-05-03 NRC INSPECTION CONDUCTED JANUARY26, 1992-FEBRUARY 29) 1992 INSPECTION REPORT NOS. 50-528, 529, AND 530/92-05

i

RESTATEMENT OF NOTICE OF VIOLATIONS50-528 92-05-02 50-528 92-0541 AND 50-528 92-05-03 During an NRC inspection conducted on January 26 through February 29, 1992, three violations of NRC requirements were identified.

In accordance with the "General Statement of Policy and Procedure for NRC Enforcement Action," 10 CFR Part 2, Appendix C, the violations are listed below:

A.

Unit 1 Technical Specification 6.8.1 states, in part, that written procedures shall be established, implemented, and maintained covering the activities recommended in Appendix A of Regulatory Guide 1.33, Revision 2, February, 1978.

Regulatory Guide 1.33, Revision 2, Appendix A, recommends surveillance procedures and general plant operating procedures.

Surveillance procedure 36ST-9SB02, "PPS Bistable Trip Units Functional Test," Step 8.11.6.2, requires the test performer to "ensure LO SG2 PRESS Trip Setpoint (Parameter

12) is at the MAXIMUMVALUEwhen in Mode 1 or
2. Adjust as necessary."

Contrary to the above, on February 4, 1992, when performing step 8.11.6.2, the test performer failed to ensure the LO SG2 PRESS trip setpoint (parameter

12) was at the maximum value when the unit was in Mode 1, resulting in the setpoint being approximately 50 pounds per square inch less that [sic] the minimum value allowed by Technical Specifications 2.2.1 and 3.3.2.

2.

General operating procedure 40DP-90P05, "Control Room Data Sheet Instructions,

" Step 2.3.2, requires that a reactor operator report "any abnormal and/or unusual condition" while fillingout the Control Room Data Sheets.

Contrary to the above, on February 4, 1992, at 5:00 pm, while fillingout the Control Room Data Sheets, the reactor operator failed to note that the 42 steam generator low pressure setpoint was incorrectly set.

This is a Severity Level IV Violation (Supplement I) applicable to Unit 1.

B.

Unit 1 Technical Specification 6.8.1 states, in part, that written procedures shall be established, implemented, and maintained covering the applicable procedures recommended in Appendix Aof Regulatory Guide 1.33, Revision 2, February 1978.

Page 1

Regulatory Guide 1.33, Appendix A; recommends procedures for performing maintenance and states that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.

Licensee Procedure 36MT-9RI06, 'VNhdrawal of ICICables," Section 8.4.5, requires the control element assembly (CEA) hoist to be used when withdrawing fixed incore instruments (ICls) for refueling operations.

Contrary to the above, on February 25, 1992, the licensee failed to implement Procedure 36MT-9RI06, in that fixed ICI455 was manually withdrawn without using the CEA hoist.

This is a Severity Level IV violation (Supplement I) applicable to Unit 1.

C.

10 CFR 50, Appendix B, Criterion XII, requires that measures be established to assure that tools, gages, instruments, and other measuring and testing devices used in activities affecting quality are properly controlled, calibrated, and adjusted at specified periods to maintain accuracy within necessary limits.

Contrary to the above, no measures were established to assure that calibration gas used for performance of containment hydrogen monitor surveillance tests, an activity affecting quality, was properly controlled and calibrated.

Specifically, on February 11,

1992, the Unit 2 Containment Hydrogen Monitor Channel A

surveillance test (Procedure 36ST-9HP03) was performed using a calibration gas that was not procured from a QA approved vendor and no other QA controls were provided to assure the proper calibration of the gas.

On February 13, 1992, one containment hydrogen monitor each in Units 1 and 3, were also determined to have had surveillance tests performed with calibration gas that was not properly controlled or calibrated.

This is a Severity Level IV violation (Supplement

1) applicable to Units 1, 2 and 3.

Page 2

ATTACHMENT1 REPLY TO NOTICE OF VIOLATIONS 50-528/92-05-02, 50-528/92-05-0 t AND 50-528/92-05-03 NRC INSPECTION CONDUCTED JANUARY26, 1992-FEBRUARY 29, 1992 INSPECTION REPORT NOS. 50-528, 529, 530/92-05

0 REPLY TO NOTICE OF VIOLATION50-528 92-05-02 Reason For The Violation The reason for both examples of the violation was a cognitive personnel error.

During scheduled surveillance testing of the Unit 1, number 1 steam generator low steam generator pressure trip setpoint on February 4, 1992, the RPS/ESFAS channel

'B'ow steam generator pressure trips for both the number 1 and number 2 steam generators were placed in bypass, as required by 36ST-9SB02, "PPS Bistable Trip Units Functional Test."

During this surveillance, the low steam generator pressure setpoint reset button was depressed, as required, resulting in the channel 'B'ow steam generator pressure trip setpoint for both steam generators being reduced to approximately 200 psia e

below the actual steam generator pressures.

The surveillance test subsequently requires resetting of the channel 'B'ow steam generator pressure trip setpoint to verify proper operation.

The channel 'B'ow steam generator pressure trip setpoint for the number 1

steam generator was reset in accordance with the surveillance test procedure.

While checking the channel 'B'ow steam generator pressure trip setpoint for the number 2 steam generator, the maintenance I&Ctechnician performing the surveillance test did not select the number 2 steam generator low steam generator pressure setpoint on the select switch. This resulted in the maintenance l&Ctechnician erroneously using the previously verified number 1 steam generator channel 'B'ow steam generator pressure trip setpoint to check the numbers 2 steam generator channel 'B'ow steam generator pressure trip setpoint.

The RPS/ESFAS channel '8'ow steam generator Page 1 of 11

pressure trips for both the number 1 and number 2 steam generators were taken out of bypass following completion of the applicable portion of the surveillance test.

N Approximately'one-half hour after the channel 'B'ow steam generator pressure trips were taken out of bypass, a Unit 1 control room reactor operator checked the low steam generator pressure trip setpoints as part of a scheduled setpoint check.

The operations procedure for control room data sheets (40DP-9OP05, "Control Room Data Sheet Instructions" ) requires any abnormal and/or unusual conditions or readings be reported to the Shift Supervisor or Assistant Shift Supervisor.

The control room reactor operator did not identify that the RPS/ESFAS channel 'B'ow steam generator pressure trip setpoint forthe number 2 steam generator was below the minimum allowed Technical Specification value, as required.

Corrective Ste s That Have Been Taken And The Results Achieved Approximately one hour after the control room reactor operator failed to identify the incorrect RPS/ESFAS channel 'B'ow steam generator pressure trip setpoint for the Unit 1, number 2 steam generator, the Assistant Shift Supervisor discovered that the setpoint was below the minimum allowed Technical Specification value. The channel

'B'ow steam generator pressure trip for the number 2 steam generator was declared inoperable and the Unit 1 maintenance l&C department was notified.

The low steam generator pressure trip setpoint was reset to the required value approximately one hour later.

Page 2 of 11

A Condition Report/Disposition Request was initiated to conduct an investigation of this event and subsequently determined the cause to be personnel error.

The involved control room reactor operator and maintenance I8 C technician have been disciplined in accordance with the APS Positive Discipline Program.

A control room night order discussing this event was issued in Units 1, 2, and 3 to reinforce the importance of attention to detail in performing routine checks thoroughly.

Briefings have been conducted on this event with Units 1, 2, and 3 maintenance l&C technicians.

As an enhancement, the surveillance test procedure (36ST-9SB02) has been revised to add detailed action steps to direct performers on how to attain and determine the low steam generator pressure trip setpoints for added assurance that the minimum e

allowed value for the trip setpoint is attained prior to removing the low steam generator pressure trip from bypass.

The investigation results were provided to the NRC in a letter from James M.

Levine dated March 5, 1992 (Licensee Event Report 528/92-003-00).

Corrective Ste s That Will Be Taken To Avoid Further Violations The corrective actions discussed above are considered adequate to avoid further violations and no additional corrective actions are planned.

Page 3of11

~

Date When Full Com Ilance Will Be Achieved Full compliance was achieved on February 4, 1992, upon restoring the Unit 1, steam generator number 2 low steam generator pressure trip setpoint.to the minimum allowed Technical Specification value.

Additional Information The inspection report cover letter requests an assessment of the need for independent verification of the reactor trip setpoints adjusted during surveillance testing.

During the investigation of this event, APS evaluated the need for independent verification of as-left reactor trip setpoints.

Although no previous examples of improper restoration of reactor trip setpoints at the conclusion of surveillance testing were identified, APS e

concluded that an additional check of as-left reactor trip setpoints would be prudent, if the setpoint was. adjusted outside the acceptance criteria during the surveillance test.

Surveillance testing meeting this criteria was identified for the low steam generator pressure trip and the low pressurizer pressure trip.

Changes to the PPS bistable trip units functional test procedure (36ST-9SB02) have been initiated to require a separate check to verifythat the low steam generator pressure trip setpoint and the low pressurizer pressure trip setpoint are within their acceptance criteria prior to removing the trips from bypass.

These changes will be implemented by June 30, 1992.

Page 4 of 11

REPLY TO NOTICE OF VIOLATION50-528 92-05-01 Reason For The Violation The reason for the violation was an improper procedural step and subsequent implementation of the flexibilityallowed by the step.

Prior to February 25, 1992, during Unit 1 refueling activities, sixty incore instruments

,(ICIs) had been withdrawn in accordance with maintenance procedure 36MT-9RI06, "Withdrawal OfThe Incore Instruments For Reactor Refueling Operations," leaving one ICI installed. On February 25, 1992, scaffolding had been erected at the entrance to the east end of the refueling canal.

This scaffolding prevented placement of the control element assembly (CEA)/ICI change platform above the ICI holding frame, and consequently the use of the CEA hoist to withdraw the final ICI, as required by 36MT-9RI06, Step 8.4.5. The a

involved Work Group Supervisor reviewed 36MT-9RI06 for an alternate means to remove the final ICI. Step 7.7 of 36MT-9RI06 states, 'This procedure should be considered a

guideline, the I&C technician and Work Group Supervisor should have flexibilityin the order of work performance and should decide the need for some steps depending upon inspection results, such as cleaning of slip tubes, spacers, etc. ".

The Work Group Supervisor interpreted this step as allowing a manual withdrawal of an ICI, in lieu of using the CEA hoist, as required by 36MT-9RI06, Step 8.4.5.

Following the decision to attempt a manual withdrawal of the final ICI, a tailboard meeting was conducted, at which the ICI task shift lead was cautioned on the slow lift requirement and the 500 pound maximum pull requirement of 36MT-9RI06. The radiation Page 5 of 11

0 protection department was notified of the planned ICI manual withdrawal.

. During the actual ICI withdrawal, a rope was attached to the ICI lift bail and used by a technician on the 140 foot elevation platform to withdraw the ICI.

A second technician, in the accompaniment of a radiation protection technician, was located in the refuel cavity to wipe the cable as it was withdrawn.

When the withdrawal was first attempted, the force was greater than anticipated, so the technicians stopped the withdrawal attempt to investigate the cause.

A piece of duct tape was removed from the ICI cable and the ICI was successfully withdrawn and secured in the ICI holding frame The duct tape had been left following a preceding, unrelated maintenance activity to replace the ICI seal housing.

Corrective Ste s That Have Been Taken And The Results Achieved A Condition Report/Disposition Request was initiated to investigate this activity and determined the cause discussed above.

The B&W Nuclear Services personnel were briefed on the incident and the need for verbatim procedural compliance was emphasized.

Changes have been made to maintenance procedure 36MT-BRI06, 'Withdrawal Of The Incore Instruments For Reactor Refueling Operations," to delete the phrase, "this procedure should be considered a guideline," from Step 7.7 (Step renumbered as 2.1.2.7) and to revise Step 8.4,5 (Step renumbered as 4.4.12) to allow lifting ICls manually.

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0 Corrective Ste s That Will Be Taken To Avoid Further Violations The corrective actions discussed above are considered adequate to avoid further violations and no additional corrective actions are planned.

Date When Full Com Ilance Will Be Achieved Full compliance was achieved on February 25, 1992, upon completion of the manual withdrawal of the final Unit 1 ICI.

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REPLY TO NOTICE OF VIOLATION50-528 92-05-03 Reason For The Violation The reason for the violation was inadequate interim corrective measures upon identification of a quality deficiency.

Aquality deficiency report was initiated in April, 1991, to document that surveillance test procedure 36ST-9HP03, "Containment Hydrogen Monitoring System Calibration Test, Channel A," was inadequate in that the test gas used was not traceable to a calibration standard.

An action plan was developed to address this deficiency which included actions to establish technical specification and quality requirements for the test gas and locate an acceptable vendor. The test gas used in this surveillance was being purchased on a non-quality related purchase order used to purchase miscellaneous gases, without identifying specific plant applications for each gas.

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Prior to an acceptable vendor being approved, interim measures were taken to ensure the quality of the test gas used in the performance of 36ST-9HP03. A prospective vendor (Air Products and Chemical) was selected based on their use by another Region V utilityas a supplier of safety-related calibration gases.

The prospective vendor's quality assurance manual was reviewed and APS concluded that the vendor had adequate processes for ensuring that the required calibration standards are accurately represented in their Certificates of Analysis (CQA). APS also verified that the test gas being supplied by a local vendor was, in fact, being filled by Air Products and Chemical.

Surveillance test procedures, 36ST-9HP03 and 36ST-9HP04 (Containment Hydrogen Monitoring Page 8of11

System Calibration Test, Channel B) were revised to require the serial number on the test gas bottle to be recorded during performance of the hydrogen monitoring system

'urveillance test to provide traceability of the gas bottle.

Following identification of the critical design attributes that are essential to the dedication process of test gas, APS performed a commercial grade survey of AirProducts and Chemical and identified some minor programmatic issues, none of which would question the accuracy of the hydrogen concentration.

A randomly selected bottle of test gas filled by this vendor which had been supplied to APS was verified to contain the correct hydrogen concentration during this survey.

On January 9, 1992, due to an urgent need for hydrogen test gas, the system engineer and the Unit 1 l&Cmaintenance department authorized a purchase of hydrogen e

test gas filled by a local vendor using the existing non-quality related purchase order. No test gas was in stock at APS and approximately two weeks would have been necessary to obtain the test gas from Air Products and Chemical.

Test gas was obtained from the local vendor and used in Unit 1. Although use of hydrogen test gas filled by the local vendor in a hydrogen monitoring system surveillance test was inappropriate, involved personnel did comply with interim corrective measures.

During the week of February 10, 1992, an NRC inspector was observing the hydrogen monitoring system surveillance test on a Unit 2 hydrogen analyzer and noted that the test gas being used was not traceable to the vendor being evaluated for acceptance by APS.

Based on this observation, all three units were checked for hydrogen test gas bottles which were not traceable to the vendor being evaluated for acceptance.

Three additional test gas bottles were found, Page 9 of 11

which were not traceable to the vendor being evaluated for acceptance.

These bottles had been purchased under the non-quality related purchase order for miscellaneous gases and filled by a local vendor at various times.

Corrective Ste s That Have Been Taken and Results Achieved Hydrogen test gas bottles which were filled by the local vendor were removed from service, quarantined, and subsequently returned to the vendor.

Hydrogen monitoring system surveillance tests were performed on the hydrogen analyzers which had been tested using test gas bottles filled by the local vendor using test gas bottles filled by Air Products and Chemical.

The tests required no adjustments to hydrogen analyzers, thus validating the tests performed using test gas bottles filled by H

the local vendor.

AirProducts and Chemical has been accepted by APS as capable of providing test gases of the required'quality and placed on the Commercial Grade Approved Vendor's List.

A quality related purchase order has been issued to Air Products and Chemical to establish a new stock level of test gases.

The procurement/warehouse tracking (class and item) numbers for test gas have been input into the Materials Management Information System and Station Information Management System for inclusion in corrective maintenance and surveillance test work order packages associated with'hydrogen analyzers.

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Corrective S e s That Will Be Taken To Avoid Further Violations The corrective actions discussed above are considered adequate to avoid further violations and no additional corrective actions are planned.

Date When Full Com liance Will Be Achieve Full compliance was achieved on February 14, 1992, upon replacement of the identified test gas bottles which had been filled by the local vendor with test gas bottles filled by Air Products and Chemical.

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