IR 05000335/2018010: Difference between revisions

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=Text=
=Text=
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION une 20, 2018
{{#Wiki_filter:June 20, 2018


==SUBJECT:==
==SUBJECT:==
ST. LUCIE PLANT - NUCLEAR REGULATORY COMMISSION PROBLEM IDENTIFICATION AND RESOLUTION INSPECTION REPORT 05000335/2018010 AND 05000389/2018010
ST. LUCIE PLANT - NUCLEAR REGULATORY COMMISSION PROBLEM  
 
IDENTIFICATION AND RESOLUTION INSPECTION REPORT  
 
05000335/2018010 AND 05000389/2018010


==Dear Mr. Nazar:==
==Dear Mr. Nazar:==
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Sincerely,
Sincerely,
/RA/
/RA/  
Randall A. Musser, Chief Reactor Projects Branch 3 Division of Reactor Projects Docket Nos.: 50-335, 50-389 License Nos.: DPR-67, NPF-16
 
Randall A. Musser, Chief  
 
Reactor Projects Branch 3  
 
Division of Reactor Projects  
 
Docket Nos.: 50-335, 50-389 License Nos.: DPR-67, NPF-16  


===Enclosure:===
===Enclosure:===
IR 05000335/2018010 and 05000389/2018010
IR 05000335/2018010 and 05000389/2018010  


REGION II==
REGION II==
Docket Nos.: 50-335, 50-389 License Nos.: DRP-67, NPF-16 Report Nos.: 05000335/2018010, 05000389/2018010 Enterprise Identifier: I-2018-010-0045 Licensee: Florida Power & Light Company (FPL)
Docket Nos.:
Facility: St. Lucie Plant, Units 1 and 2 Location: 6501 South Ocean Drive Jensen Beach, FL 34957 Dates: May 7 through May 25, 2018 Inspectors: A. Wilson, Project Engineer, Team Leader L. Pressley, Senior Project Engineer S. Roberts, Resident Inspector J. Rotton, Senior Resident Inspector Approved by: Randall A. Musser, Chief Reactor Projects Branch 3 Division of Reactor Projects Enclosure
50-335, 50-389  
 
License Nos.:
DRP-67, NPF-16  
 
Report Nos.:
05000335/2018010, 05000389/2018010  
 
Enterprise Identifier: I-2018-010-0045  
 
Licensee:  
 
Florida Power & Light Company (FPL)  
 
Facility:  
 
St. Lucie Plant, Units 1 and 2  
 
Location:  
 
6501 South Ocean Drive Jensen Beach, FL 34957  
 
Dates:  
 
May 7 through May 25, 2018  
 
Inspectors:  
 
A. Wilson, Project Engineer, Team Leader L. Pressley, Senior Project Engineer S. Roberts, Resident Inspector J. Rotton, Senior Resident Inspector  
 
Approved by:
Randall A. Musser, Chief Reactor Projects Branch 3 Division of Reactor Projects


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a Problem Identification and Resolution Inspection at St. Lucie Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a Problem Identification and Resolution Inspection at St. Lucie Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.


List of Findings and Violations No findings were identified.
===List of Findings and Violations===
No findings were identified.


=INSPECTION SCOPE=
=INSPECTION SCOPE=
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==REACTOR SAFETY==
==REACTOR SAFETY==
===71152B - Problem Identification and Resolution===
{{IP sample|IP=IP 71152|count=1}}


===71152B - Problem Identification and Resolution ===
{{IP sample|IP=IP 71152|count=1}}
The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety-conscious work environment. The assessment is documented below.
The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety-conscious work environment. The assessment is documented below.
: (1) Corrective Action Program Effectiveness: Problem Identification, Problem Prioritization and Evaluation, and Corrective Actions - The inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs.
: (1) Corrective Action Program Effectiveness: Problem Identification, Problem Prioritization and Evaluation, and Corrective Actions - The inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs.
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==INSPECTION RESULTS==
==INSPECTION RESULTS==
Corrective Action Program Effectiveness Observations                 71152Problem Identification and Resolution Based on the samples reviewed, the team determined that the licensees corrective action program (CAP) complied with regulatory requirements and self-imposed standards. The licensees implementation of the CAP adequately supported nuclear safety.
Corrective Action Program Effectiveness Observations 71152Problem Identification and Resolution Based on the samples reviewed, the team determined that the licensees corrective action program (CAP) complied with regulatory requirements and self-imposed standards. The licensees implementation of the CAP adequately supported nuclear safety.


Effectiveness of Problem Identification: The inspectors determined that the licensee was effective in identifying problems and entering them into the CAP and there was a low threshold for entering issues into the CAP. This conclusion was based on a review of the requirements for initiating Condition Reports (CRs) as described in licensee procedure PI-AA-104-1000, Condition Reporting, and managements expectation that employees were encouraged to initiate CRs for any reason. Additionally, site management was actively involved in the CAP and focused appropriate attention on significant plant issues.
Effectiveness of Problem Identification: The inspectors determined that the licensee was effective in identifying problems and entering them into the CAP and there was a low threshold for entering issues into the CAP. This conclusion was based on a review of the requirements for initiating Condition Reports (CRs) as described in licensee procedure PI-AA-104-1000, Condition Reporting, and managements expectation that employees were encouraged to initiate CRs for any reason. Additionally, site management was actively involved in the CAP and focused appropriate attention on significant plant issues.
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For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence. The team reviewed performance indicators, CRs, and effectiveness reviews, as applicable, to verify that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence (CAPRs) were sufficient to ensure corrective actions were properly implemented and were effective.
For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence. The team reviewed performance indicators, CRs, and effectiveness reviews, as applicable, to verify that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence (CAPRs) were sufficient to ensure corrective actions were properly implemented and were effective.


Minor Performance Deficiency                           71152Problem Identification and Resolution Minor Performance Deficiency: The station failed to properly consider mission time of EDGs in operability evaluations in accordance with Procedure EN-AA-203-1001. Specifically, as documented in several CRs, the conclusions provided within the operability analysis sections could not be supported without evaluating the conditions against the system mission time.
Minor Performance Deficiency 71152Problem Identification and Resolution Minor Performance Deficiency: The station failed to properly consider mission time of EDGs in operability evaluations in accordance with Procedure EN-AA-203-1001. Specifically, as documented in several CRs, the conclusions provided within the operability analysis sections could not be supported without evaluating the conditions against the system mission time.


The inspectors reviewed CRs 2132695, 2132704, and 2132705, which were all initiated to document oil leaks on the EDGs. Each CR contained a statement that, there is no impact on the ability of the EDG to meet its mission time, under the operability notes.
The inspectors reviewed CRs 2132695, 2132704, and 2132705, which were all initiated to document oil leaks on the EDGs. Each CR contained a statement that, there is no impact on the ability of the EDG to meet its mission time, under the operability notes.
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Screening: The inspectors screened the issue in accordance with Inspection Manual Chapter 0612, Appendix B, Issue Screening, and determined that the performance deficiency did not meet the criteria in Block 3 to be a More-than-Minor issue. The inspectors determined that the CRs reviewed for this instance were minor in nature and therefore would unlikely change the outcome of the operability determinations of the examples reviewed. The inspectors did not identify a violation of regulatory requirements associated with this minor performance deficiency.
Screening: The inspectors screened the issue in accordance with Inspection Manual Chapter 0612, Appendix B, Issue Screening, and determined that the performance deficiency did not meet the criteria in Block 3 to be a More-than-Minor issue. The inspectors determined that the CRs reviewed for this instance were minor in nature and therefore would unlikely change the outcome of the operability determinations of the examples reviewed. The inspectors did not identify a violation of regulatory requirements associated with this minor performance deficiency.


Operating Experience and Self-Assessments and Audits Observations           71152Problem Identification and Resolution Based on the samples reviewed, the team determined that stations processes for the use of industry and NRC operating experience information and for the performance of audits and self-assessments were effective and complied with all regulatory requirements and licensee standards. The implementation of these programs adequately supported nuclear safety.
Operating Experience and Self-Assessments and Audits Observations 71152Problem Identification and Resolution Based on the samples reviewed, the team determined that stations processes for the use of industry and NRC operating experience information and for the performance of audits and self-assessments were effective and complied with all regulatory requirements and licensee standards. The implementation of these programs adequately supported nuclear safety.


Overall, the team concluded that operating experience was adequately evaluated for applicability and that appropriate actions were implemented to address lessons learned as needed. In general, the inspectors determined that the licensee was effective at performing self-assessments and audits to identify issues at a low level, properly evaluated those issues, and resolved them commensurate with their safety significance.
Overall, the team concluded that operating experience was adequately evaluated for applicability and that appropriate actions were implemented to address lessons learned as needed. In general, the inspectors determined that the licensee was effective at performing self-assessments and audits to identify issues at a low level, properly evaluated those issues, and resolved them commensurate with their safety significance.


Safety Conscious Work Environment Observations                   71152Problem Identification and Resolution Based on interviews with plant staff and reviews of the latest safety culture survey results to assess the safety-conscious work environment on site, the team found no evidence of challenges to safety-conscious work environment. Employees appeared willing to raise nuclear safety concerns through at least one of the several means available.
Safety Conscious Work Environment Observations 71152Problem Identification and Resolution Based on interviews with plant staff and reviews of the latest safety culture survey results to assess the safety-conscious work environment on site, the team found no evidence of challenges to safety-conscious work environment. Employees appeared willing to raise nuclear safety concerns through at least one of the several means available.


==EXIT MEETINGS AND DEBRIEFS==
==EXIT MEETINGS AND DEBRIEFS==
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=DOCUMENTS REVIEWED=
=DOCUMENTS REVIEWED=


Condition Reports
Condition Reports  
  - 1893969; Replace All 9 Bus Vent Covers on 1A UAT; 8/2/2013
-
  - 1920696; Unit 2 Manual Reactor Trip; 11/14/2013
1893969; Replace All 9 Bus Vent Covers on 1A UAT; 8/2/2013  
  - 1920742; Found Degraded Relays During Extent of Condition; 11/15/2013
-
  - 1937045; HCV-14-11A1 Seal Cooler Valve Failed Closed; 1/29/2014
20696; Unit 2 Manual Reactor Trip; 11/14/2013  
  - 1948469; V381 Over Thrust During Disk Pull Out; 3/15/2014
-
  - 1951584; Degraded Contacts Prevented 2B EDG Breaker From Closing; 3/25/2014
20742; Found Degraded Relays During Extent of Condition; 11/15/2013  
  - 1973521; LPM Channel 1 Below Minimum Threshold; 6/20/2014
-
  - 2054489 'B' RPS CNTMT Press Bistable Trip & Pre-Trip Lights Inop; 06/16/2015
1937045; HCV-14-11A1 Seal Cooler Valve Failed Closed; 1/29/2014  
  - 2077661; 2C ICW Pp Motor Tripped On Overcurrent; 9/30/2015
-
  - 2083954; Indicator Stuck At The Top Of The Gauge; 10/23/2015
1948469; V381 Over Thrust During Disk Pull Out; 3/15/2014  
  - 2084836; 2C AFW Pump Governor Oil Leak; 10/23/2015
-
  - 2090225; Unauthorized entry into a High Radiation area; 5/3/2016
1951584; Degraded Contacts Prevented 2B EDG Breaker From Closing; 3/25/2014  
  - 2095560; U1 Circ Water DFS Filter DF-21-1B1 High DP Condition; 12/5/2015
-
  - 2108156; EDG 1A One Engine Fail To Start Alarm Locks In During Surv; 02/06/2016
1973521; LPM Channel 1 Below Minimum Threshold; 6/20/2014  
  - 2108868; 2016 CDBI Functionality of EER Sup Fan Discharge Dampers, GD-1/2;
-
2/9/2016
2054489 'B' RPS CNTMT Press Bistable Trip & Pre-Trip Lights Inop; 06/16/2015  
  - 2109116; 2016 CDBI HVAC Action in 1-EOP-09; 2/10/2016
-
  - 2109310; Hydrogen Purity Local Meter Not Indicating Correct Purity; 2/11/2016
2077661; 2C ICW Pp Motor Tripped On Overcurrent; 9/30/2015  
  - 2111358; Failure to verify adequacy of Unit 1 Electrical Equipment room ventilation
-
system; 04/11/2016
2083954; Indicator Stuck At The Top Of The Gauge; 10/23/2015  
  - 2112128; Reverse Flow & Backward Rotation Observed on HVS-5A/B
-
  - 2114645; 10 CFR Part 21 issue for Masterpack NT & NW breakers; 1/18/2017
2084836; 2C AFW Pump Governor Oil Leak; 10/23/2015  
  - 2117193; Failure to verify adequacy of Unit 1 Electrical Equipment room ventilation
-
system; 04/11/2016
2090225; Unauthorized entry into a High Radiation area; 5/3/2016  
  - 2125717; ACE to Address Green NCV on CAQ for EER Supply Fans; 7/14/2016
-
  - 2128716; Loose Parts Monitoring Alarm For Channel 4; 4/29/2016
2095560; U1 Circ Water DFS Filter DF-21-1B1 High DP Condition; 12/5/2015  
  - 2129351; Control Room Shift Communicator failure on simulator; 5/2/2016
-
  - 2131209; "A" EDG Conduit Covers Loose; 5/11/2016
2108156; EDG 1A One Engine Fail To Start Alarm Locks In During Surv; 02/06/2016  
  - 2131211; "A" EDG Conduit Termination Pulled Loose; 5/11/2016
-
  - 2131215; 1A EDG Set Instrument Tubing In Contact With Each Other; 5/11/2016
2108868; 2016 CDBI Functionality of EER Sup Fan Discharge Dampers, GD-1/2;
  - 2131219; 1A1 EDG Machine Screw Found Out Of Place; 5/11/2016
2/9/2016  
  - 2132695; Valve Gallery Cover On 1A2 EDG Leaking Oil; 5/18/2016
-
  - 2132704; 1A1 EDG Turbocharger Flange Oil Leak; 5/18/2016
2109116; 2016 CDBI HVAC Action in 1-EOP-09; 2/10/2016  
  - 2132705; 1A1 EDG Camshaft Covers Leaking Oil; 5/18/2016
-
  - 2133018; UNIT 2 2A2 EDG Fuel Pressure Low; 5/19/2016
2109310; Hydrogen Purity Local Meter Not Indicating Correct Purity; 2/11/2016  
  - 2133422; 2B MSIV accumulator corrosion; 5/22/2016
-
  - 2133504; 2D Instrument air compressor not loading; 5/23/2016
2111358; Failure to verify adequacy of Unit 1 Electrical Equipment room ventilation
  - 2133774; 2D Instrument air compressor trip on high cylinder temperature; 5/24/2016
system; 04/11/2016  
  - 2134435; NOS Finding - Radioactive material stored outdoors; 5/26/2016
-
  - 2135100; 1A EDG MVAR Readings Off Normal; 5/31/2016
2112128; Reverse Flow & Backward Rotation Observed on HVS-5A/B  
  - 2135780; NRC EQ Inspection - Containment High Range Radiation Monitors; 6/2/2016
-
  - 2136211; TR-1112 Failed Low Affecting DCS and A QSPDS; 6/6/2016
2114645; 10 CFR Part 21 issue for Masterpack NT & NW breakers; 1/18/2017  
  - 2136427; ROTORK Controls, Inc. and Electroswitch Part 21 issues; 6/7/2016
-
  - 2137373; DCS Point 2CSFM 10:P8023a A.PNT; 6/10/2016
2117193; Failure to verify adequacy of Unit 1 Electrical Equipment room ventilation
  - 2140294; 2D Instrument air compressor trip during performance run; 6/24/2016
system; 04/11/2016  
  - 2140595; 1A EDG MVAR Swings; 6/27/2016
-
  - 2143046; U2 RCS Zinc concentration dropped below threshold limit; 7/12/2016
25717; ACE to Address Green NCV on CAQ for EER Supply Fans; 7/14/2016  
  - 2143242; Evaluation of U2 ACC-3C refrigeration migration issue; 7/12/201
-
- 2144201; Shortfall in observations of Radiological work practices; 7/17/2016
28716; Loose Parts Monitoring Alarm For Channel 4; 4/29/2016  
- 2144412; 1A Fire pump breaker,1-40209, 10 CFR Part issue; 7/18/2016
-
- 2144416; 2AB to 2B2 bus tie breaker, 2-40706, 10 CFR Part 21 issue; 7/18/2016
29351; Control Room Shift Communicator failure on simulator; 5/2/2016  
- 2145831; Condition of RABS unsat; 7/25/2016
-
- 2146175; U1 RCS Zinc concentration less than admin limit; 7/27/2016
2131209; "A" EDG Conduit Covers Loose; 5/11/2016  
- 2148252; V3217 Backleakage During Shutdown Cooling Flush; 8/6/16
-
- 2149500; Mv-09-11 Only Strokes Closed Intermittently; 8/12/2016
2131211; "A" EDG Conduit Termination Pulled Loose; 5/11/2016  
- 2150868; Work hours control violation; 8/18/2016
-
- 2151322; Inadequate Modification Of The Unit 2 DOST, EC274456; 8/22/2016
2131215; 1A EDG Set Instrument Tubing In Contact With Each Other; 5/11/2016  
- 2151502; High Radiation Area and contamination area created due to RES; 8/23/2016
-
- 2152647; Instrument air system pressure degrading trend; 8/28/2016
2131219; 1A1 EDG Machine Screw Found Out Of Place; 5/11/2016  
- 2154938; All NRC ENS phone lines OOS; 9/9/2016
-
- 2155627; Untimely classification resulting in missed DEP-PI; 9/13/2016
2132695; Valve Gallery Cover On 1A2 EDG Leaking Oil; 5/18/2016  
- 2156690; Recovery plan for exercise and drill performance; 9/19/2016
-
- 2156817; DEP miss due to inaccurate state notification during SIMEVAL; 9/20/2016
2132704; 1A1 EDG Turbocharger Flange Oil Leak; 5/18/2016  
- 2157214; 1B DC Bus Ground Locked In; 9/21/2016
-
- 2157980; Core Exit Thermocouple 16 Q-3, Continues To Drop Out Low; 09/25/2016
2132705; 1A1 EDG Camshaft Covers Leaking Oil; 5/18/2016  
- 2158314; U1 CCW Tritium greater than MDA; 9/27/2016
-
- 2160390; 1B EDG Room Floor Drain Backing Up; 10/5/2016
2133018; UNIT 2 2A2 EDG Fuel Pressure Low; 5/19/2016  
- 2165042; Foamy oil in U1 ACC-3C, control room air conditioner; 10/25/2016
-
- 2165690; 1A EDG MVAR Swings During Adjustments; 10/27/2016
2133422; 2B MSIV accumulator corrosion; 5/22/2016  
- 2166772; Industry OE - Harris NOUE (LOOP); 11/1/2016
-
- 2166950; EDG LOOP Response Time Safeguards Acceptance Criteria; 11/1/2016
2133504; 2D Instrument air compressor not loading; 5/23/2016  
- 2167267; Industry OE - Farley Alert due to toxic gas; 11/3/2016
-
- 2168328; Leakage Past V09248; 11/9/2016
2133774; 2D Instrument air compressor trip on high cylinder temperature; 5/24/2016  
- 2168775; Industry OE - Dresden U3 Alert- ICES Report# 323383; 11/11/2016
-
- 2168864; WO: 40499100-01 Inadvertently Closed In EWP; 11/11/2016
2134435; NOS Finding - Radioactive material stored outdoors; 5/26/2016  
- 2174203; Loose Parts Monitor Alarming; 12/12/2016
-
- 2175061; EDG Starting Air Leakage Test Margin Recovery; 12/15/2016
2135100; 1A EDG MVAR Readings Off Normal; 5/31/2016  
- 2175530; During Sl-1-27, V09280 Was Worked And PMT Was Not Completed;
-
2/15/2016
2135780; NRC EQ Inspection - Containment High Range Radiation Monitors; 6/2/2016  
- 2175641; L-31, Boron Concentration Low Channel 1 Alarming; 12/17/2016
-
- 2176118; Inappropriate long term storage of radioactive material; 12/21/2016
2136211; TR-1112 Failed Low Affecting DCS and A QSPDS; 6/6/2016  
- 2179806; 2D Instrument air compressor excessive cycling; 1/14/2017
-
- 2181204; Declining RCA Radiation Worker observation trend; 1/23/2017
2136427; ROTORK Controls, Inc. and Electroswitch Part 21 issues; 6/7/2016  
- 2183774; ALARA near miss due to inadequate scaffold; 2/4/2017
-
- 2184494; PSL Siren S-70 test failure; 2/8/2017
2137373; DCS Point 2CSFM 10:P8023a A.PNT; 6/10/2016  
- 2185542; Waste processing challenges due to U1 AWST Activity; 2/14/2017
-
- 2186438; HVA/ACC-3B Freon leak; 2/17/2017
2140294; 2D Instrument air compressor trip during performance run; 6/24/2016  
- 2187133; 2B EDG Jacket Water Temp Low During Safeguards; 2/21/17
-
- 2187169; OE regarding a loss of instrument air (NRC IN 2016-05); 2/22/2017
2140595; 1A EDG MVAR Swings; 6/27/2016  
- 2187670; AFW PP 1C-PP OTBD Brg Wear-Increased Particle Concentration; 2/23/2017
-
- 2188004; Personnel contamination event / PCE #17-013; 2/25/2017
2143046; U2 RCS Zinc concentration dropped below threshold limit; 7/12/2016  
- 2188010; The Wrong Pc Level Oil Was Used In The 1c Auxiliary FW Pump; 2/25/2017
-
- 2188020; SE-07-5F Solenoid Valve PEN P-51, Field Wires Damaged; 3/1/2017
2143242; Evaluation of U2 ACC-3C refrigeration migration issue; 7/12/201  
- 2188171; Personnel contamination event / PCE #17-015; 2/26/2017
 
- 2188184; EDG Fuel Oil Cross-Connect Surveillance Conundrum; 2/27/17
-
- 2188751; Engineered Safeguard Logic Cabinet Sa Volt Meter Failed; 03/01/2017
2144201; Shortfall in observations of Radiological work practices; 7/17/2016  
- 2189467; 2A Instrument air dryer blowing down continuously; 3/4/2017
-
- 2189538; 1C Instrument air compressor low oil level; 3/5/2017
2144412; 1A Fire pump breaker,1-40209, 10 CFR Part issue; 7/18/2016  
- 2190852; 1C Instrument air compressor excessive oil consumption; 3/11/2017
-
- 2190895; 20 Gallons Of Oil Added To 2A1 Engine On 2A EDG; 3/11/2017
2144416; 2AB to 2B2 bus tie breaker, 2-40706, 10 CFR Part 21 issue; 7/18/2016  
- 2190896; 12 Gallons Of Oil Added To 2A2 Engine On 2A EDG; 3/11/2017
-
- 2192588; A Feedwater Header Mfiv,HCV-09-1,Hydraulic Actuator Issue; 3/21/2017
2145831; Condition of RABS unsat; 7/25/2016  
- 2193112; 2B2 RCP Lower Guide BRG Temp Inconsistent Output; 3/22/2017
-
- 2193490; 1C AFW Pp OTBD Oil Reservoir Drain/Flush Before Next Run; 3/24/2017
2146175; U1 RCS Zinc concentration less than admin limit; 7/27/2016  
- 2193884; 1C Instrument air compressor oil leak; 3/25/2017
-
- 2194614; 1D Instrument air compressor low oil level; 3/29/2017
2148252; V3217 Backleakage During Shutdown Cooling Flush; 8/6/16  
- 2202422; HVA/ACC-3A Low Freon level while running; 4/30/2017
-
- 2203125; Ladder laying across contaminated area boundary; 5/3/2017
2149500; Mv-09-11 Only Strokes Closed Intermittently; 8/12/2016  
- 2203233; Request Conditional Release Of R&O 150 Oil For 2B EDG; 5/4/2017
-
- 2204967; Industry OE - LaSalle Anchor Darling Part 21; 5/15/2017
2150868; Work hours control violation; 8/18/2016  
- 2205200; Unexpected Loss of the 2A3 4160V Safety Bus; 5/16/2017
-
- 2205687; U1 CCW shows signs of Tritium activity; 5/17/2017
2151322; Inadequate Modification Of The Unit 2 DOST, EC274456; 8/22/2016  
- 2205761; 2A2 EDG Tubing Found Degraded; 5/18/2017
-
- 2206260; HCV-09-2B Oil Leak; 5/21/2017
2151502; High Radiation Area and contamination area created due to RES; 8/23/2016  
- 2206286; 2A1 EDG Water Immersion Heater Tripping; 5/21/2017
-
- 2207340; Level 1 Assessment - Trending Program at PSL; 5/26/2017
2152647; Instrument air system pressure degrading trend; 8/28/2016  
- 2208096; Unit 1 TSC plant computer room air conditioning not cooling; 5/31/2017
-
23692; Incomplete actions from Hurricane Matthew assessment; 9/6/2017
2154938; All NRC ENS phone lines OOS; 9/9/2016  
- 2210364; HVA 3A trip on motor temperature overload; 6/14/2017
-
- 2212311; MCC AC-DC starter mechanical interlock reliability review; 6/26/2017
2155627; Untimely classification resulting in missed DEP-PI; 9/13/2016  
- 2217392; Engineering to perform OE review Robinson Plane OE 241354; 7/27/2017
-
- 2217631; U1 Hot Leg Injection Procedures; 7/29/2017
2156690; Recovery plan for exercise and drill performance; 9/19/2016  
- 2219154; HCV-09-2B Reservoir Oil Level Low In Spec Not An Active Leak; 8/8/2017
-
- 2220259; 2A1 EDG Fuel Pressure Reads Below Min Value; 8/14/2017
2156817; DEP miss due to inaccurate state notification during SIMEVAL; 9/20/2016  
- 2221186; HVA/ACC-3B failure due to ground on condensing unit; 8/20/2017
-
- 2222623; 1B2 EDG Needs Oil Added; 8/29/2017
2157214; 1B DC Bus Ground Locked In; 9/21/2016  
- 2222743; U1 ACC-3 thermostat not responding; 8/29/2017
-
- 2224199; MFIV Oil Reservoir At The Low Level Mark; 9/10/2017
2157980; Core Exit Thermocouple 16 Q-3, Continues To Drop Out Low; 09/25/2016  
- 2224325; Unacceptable performance for post-hurricane accountability; 9/11/2017
-
- 2226606; 2B EDG Load Transient During Performance Of 2-OSP-59.01B; 9/25/17
2158314; U1 CCW Tritium greater than MDA; 9/27/2016  
- 2227429; Fire Protection Program Implementation Cognitive Trend; 9/28/2017
-
- 2229920; 2B EDG Fuel supply; 10/12/2017
2160390; 1B EDG Room Floor Drain Backing Up; 10/5/2016  
- 2230410; Elevated contamination in room; 10/14/2017
-
- 2230610; Level 1 Assessment - Fire Protection Program Implementation; 10/16/2017
2165042; Foamy oil in U1 ACC-3C, control room air conditioner; 10/25/2016  
- 2230758; OE- Industry White finding for EDG Diode Failure Catawba; 10/17/2017
-
- 2232779; U2 C AFW Flow Transmitters Isolated; 10/25/2017
2165690; 1A EDG MVAR Swings During Adjustments; 10/27/2016  
- 2232782 1A MSL Rad Monitor Frequently Spiking Into Alarm. Inop. 10/25/17
-
- 2233080; Multiple CBCS Deficiencies Create Operator Burdens; 10/27/2017
2166772; Industry OE - Harris NOUE (LOOP); 11/1/2016  
- 2233516; Work Request Cancelled w/o Any Work Performed on Active Leak;
-
10/29/2017
2166950; EDG LOOP Response Time Safeguards Acceptance Criteria; 11/1/2016  
- 2233669; Recommended Actions From Previous AR 02110464 Not Addressed;
-
10/30/2017
2167267; Industry OE - Farley Alert due to toxic gas; 11/3/2016  
- 2234317; 2-FSG-10, Safety Injection Tank Isolation - Rev 2; 11/2/2017
-
- 2235711; U1 ACC-3B low oil level; 11/10/2017
2168328; Leakage Past V09248; 11/9/2016  
- 2236131; Tritium detected in catch basins; 11/14/2017
-
- 2237096; U1 HVA-3C compressor going into pump down; 11/20/2017
2168775; Industry OE - Dresden U3 Alert-ICES Report# 323383; 11/11/2016  
- 2238413; Part 21 Report, Fisher Information Notice 17-05; 11/30/2017
-
- 2238617; 1b AFW Pp THRST BRN Preload/Early Stage Wear - Contingency; 12/1/2017
2168864; WO: 40499100-01 Inadvertently Closed In EWP; 11/11/2016  
- 2242181; Increased Flow Coming From 2B EDG OIL LEAK; 12/27/2017
-
- 2243677; Nuc. Assurance Escalation. L1: Inadequate use of GFCI protection; 1/9/2018
2174203; Loose Parts Monitor Alarming; 12/12/2016  
  - 2243798; Water Leaking from Cell Jar Lids; 1/9/2018
-
  - 2245101; 2D Instrument air compressor motor overload; 1/18/2018
2175061; EDG Starting Air Leakage Test Margin Recovery; 12/15/2016  
  - 2245821; Low Level In Reservoir; 1/23/2018
-
  - 2246135; Inappropriate Use of MA Assignments for CAQ CRs; 1/24/2018
2175530; During Sl-1-27, V09280 Was Worked And PMT Was Not Completed;
  - 2249170; One-Hour Notification; 2/13/2018
2/15/2016  
  - 2249174; Contamination in a clean area; 2/12/2018
-
  - 2249292;1b AFW Pp Outboard Cover Guard Corroded; 02/13/2018
2175641; L-31, Boron Concentration Low Channel 1 Alarming; 12/17/2016  
  - 2249873; NRC evaluated drill 2018SAE not performed IAW drill scenario; 2/15/2018
-
  - 2249999; Nuc. Assurance Escalation. L1: Metal shavings on plant equipment;
2176118; Inappropriate long term storage of radioactive material; 12/21/2016  
2/16/2018
-
  - 2250930; PI&R Self Assessment; 2/22/2018
2179806; 2D Instrument air compressor excessive cycling; 1/14/2017  
  - 2250938; PI&R Self Assessment; 2/22/2018
-
  - 2253212; Siren #1 failure; 3/8/2018
2181204; Declining RCA Radiation Worker observation trend; 1/23/2017  
  - 2253859; 1A EDG Failed Response Time Testing; 3/13/18
-
  - 2254424; Alternate Source Supplying Load Light Will Not Illuminate; 3/15/2018
2183774; ALARA near miss due to inadequate scaffold; 2/4/2017  
  - 2254769; Higher than expected dose rates on refuel bridge; 3/19/2018
-
  - 2255082; Inadequate commercial grade dedication resulted in Part 21; 3/20/2018
2184494; PSL Siren S-70 test failure; 2/8/2017  
  - 2256602; NRC Ident: Metal Shavings, Unit 1 Vital AC SUPS and 1C HPSI; 3/28/2018
-
  - 2257037; Ris-26-13-1 Reading High Alarm; 03/30/2018
2185542; Waste processing challenges due to U1 AWST Activity; 2/14/2017  
  - 2257077; 2B2 EDG Engine Needs Oil Added; Unsafe To Do So Manually; 3/30/2018
-
  - 2257159; Through wall leak on SW line reducer weld; 3/30/2018
2186438; HVA/ACC-3B Freon leak; 2/17/2017  
  - 2257515; Personnel contamination event; 4/2/2018
-
  - 2257712; RM-26-12 failure causing 2-AOP- 26.01 entry; 4/3/2018
2187133; 2B EDG Jacket Water Temp Low During Safeguards; 2/21/17  
  - 2258467; MV-09-9 'A' AFW To 'A' S/G Failed To Control; 4/8/2018
-
  - 2258467; Mv-09-9 'A' AFW To 'A' S/G Failed To Control; 4/8/2018
2187169; OE regarding a loss of instrument air (NRC IN 2016-05); 2/22/2017  
  - 2258467; MV-09-9 'A' AFW To 'A' S/G Failed To Control; 4/8/2018
-
  - 2259242; Level 1 Assessment of Part 21 Process; 4/12/2018
2187670; AFW PP 1C-PP OTBD Brg Wear-Increased Particle Concentration; 2/23/2017  
  - 2259520; Metallic Debris on floor of U2 switchgear rooms; 4/18/2018
-
  - 2263320; PI Processbook Unable to Calculate RCS Leak Rate; 5/9/2018
2188004; Personnel contamination event / PCE #17-013; 2/25/2017  
  - 2264338; 2018 NRC PI&R Inspection EDG Mission Time; 5/15/2018
-
  - 32 Security-related CRs were reviewed during the inspection
2188010; The Wrong Pc Level Oil Was Used In The 1c Auxiliary FW Pump; 2/25/2017  
Procedures
-
  - 1-GMM-80.41; Atwood & Morrill 12 Inch Swing Check Valve Maintenance; Revision 7
2188020; SE-07-5F Solenoid Valve PEN P-51, Field Wires Damaged; 3/1/2017  
  - 1-OSP-63.13A; ESF - Staggered 36 Month Surveillance For SIAS/CIS/CSAS - Train A;
-
Revisions 32 & 33
2188171; Personnel contamination event / PCE #17-015; 2/26/2017  
  - 2-FSG-10; Safety Injection Tank Isolation; Revision 2
-
  - 2-GMM-03.02; Westinghouse 12 Inch Swing Check Valve Maintenance; Revision 2
2188184; EDG Fuel Oil Cross-Connect Surveillance Conundrum; 2/27/17  
  - 2-GMM-03.04; Westinghouse 3 Inch Swing Check Valve Maintenance; Revision 4
-
  - ADM-17.32; Structures Monitoring Program; Revision 6
2188751; Engineered Safeguard Logic Cabinet Sa Volt Meter Failed; 03/01/2017  
  - EN-AA-203-1001; Operability Determinations / Functionality Assessments; Revision 29
-
  - ER-AA-100-2002; Maintenance Rule Program Administration; Revision 6
2189467; 2A Instrument air dryer blowing down continuously; 3/4/2017  
  - ER-AA-124; Check Valve Program, Revision 1
-
  - NA-AA-200-1000; Employee Concerns Program; Revision 1
2189538; 1C Instrument air compressor low oil level; 3/5/2017  
  - PI-AA-100; Condition Assessment and Response; Revision 10
-
  - PI-AA-100-1005; Root Cause Analysis; Revision 17
2190852; 1C Instrument air compressor excessive oil consumption; 3/11/2017  
  - PI-AA-100-1006; Common Cause Evaluation; Revision 13
 
  - PI-AA-100-1007; Issue Investigation; Revision 20
-
  - PI-AA-101; Assessment and Improvement Programs; Revision 24
2190895; 20 Gallons Of Oil Added To 2A1 Engine On 2A EDG; 3/11/2017  
  - PI-AA-102-1002; Internal Operating Experience; Revision 8
-
  - PI-AA-102-1003; Sharing Operating Experience With Nuclear Industry; Revision 12
2190896; 12 Gallons Of Oil Added To 2A2 Engine On 2A EDG; 3/11/2017  
    - PI-AA-104-1000; Condition Reporting; Revision 17
-
    - PI-AA-207; Trend Coding and Analysis; Revision 13
2192588; A Feedwater Header Mfiv,HCV-09-1,Hydraulic Actuator Issue; 3/21/2017  
    - PI-AA-207-1000; Station Self-Evaluation and Trending Analysis; Revision 8
-
    - SY-AA-102-1000; Safeguards Information Program; Revision 15
2193112; 2B2 RCP Lower Guide BRG Temp Inconsistent Output; 3/22/2017  
Self-Assessments, Audits, and Trend Reports
-
    - 4Q17 PSL Self-Evaluation and Trending Analysis Report
2193490; 1C AFW Pp OTBD Oil Reservoir Drain/Flush Before Next Run; 3/24/2017  
    - 4Q17 PSL/Engineering Self-Evaluation and Trending Analysis Report
-
    - 4Q17 PSL/Maintenance Self-Evaluation and Trending Analysis Report
2193884; 1C Instrument air compressor oil leak; 3/25/2017  
    - 4Q17 PSL/Operations Self-Evaluation and Trending Analysis Report
-
    - 4Q17 PSL/Radiation Protection Self-Evaluation and Trending Analysis Report
2194614; 1D Instrument air compressor low oil level; 3/29/2017  
    - 4Q17 PSL/Security Self-Evaluation and Trending Analysis Report
-
    - Pre-NRC Problem Identification & Resolution (PI&R) Inspection Assessment
202422; HVA/ACC-3A Low Freon level while running; 4/30/2017  
    - PSL 16-002 Radiation Protection and Radwaste Audit Report; 5/26/2016
-
    - PSL 16-005 EP Audit Report; 8/10/2016
203125; Ladder laying across contaminated area boundary; 5/3/2017  
    - PSL 16-006; Operations; 9/7/2016
-
    - PSL 16-009 Chemistry Audit Report; 1/04/2017
203233; Request Conditional Release Of R&O 150 Oil For 2B EDG; 5/4/2017  
    - PSL 17-003 QA Programs Audit Report; /18/2017
-
    - PSL 17-005; Engineering Audit; 6/30/2017
204967; Industry OE - LaSalle Anchor Darling Part 21; 5/15/2017  
    - PSL 17-007 Emergency Preparedness Audit Report; 8/10/2017
-
    - PSL 17-010; Performance Improvement; 1/25/2018
205200; Unexpected Loss of the 2A3 4160V Safety Bus; 5/16/2017  
    - PSL 17-012; Time Sensitive Action Review; 12/21/2017
-
Work Orders
205687; U1 CCW shows signs of Tritium activity; 5/17/2017  
    - 40276910-01
-
    - 40276911-01
205761; 2A2 EDG Tubing Found Degraded; 5/18/2017  
    - 40284284
-
    - 40374092
206260; HCV-09-2B Oil Leak; 5/21/2017  
    - 40374094
-
    - 40398730
206286; 2A1 EDG Water Immersion Heater Tripping; 5/21/2017  
    - 40410089
-
    - 40411087
207340; Level 1 Assessment - Trending Program at PSL; 5/26/2017  
    - 40469413
-
    - 40471113
208096; Unit 1 TSC plant computer room air conditioning not cooling; 5/31/2017
    - 40472171
23692; Incomplete actions from Hurricane Matthew assessment; 9/6/2017  
    - 40477208
-
    - 40477338
210364; HVA 3A trip on motor temperature overload; 6/14/2017  
    - 40490422
-
    - 40521769
212311; MCC AC-DC starter mechanical interlock reliability review; 6/26/2017  
    - 40538193
-
    - 40591898
217392; Engineering to perform OE review Robinson Plane OE 241354; 7/27/2017  
    - 94141676
-
    - 94143832
217631; U1 Hot Leg Injection Procedures; 7/29/2017  
    - 94156308
-
    - 94172111
219154; HCV-09-2B Reservoir Oil Level Low In Spec Not An Active Leak; 8/8/2017  
Other
-
    - Alternative Analysis Unit 2 DOST NFPA 30 Section 2348 Compliance AR 2151322-10;
20259; 2A1 EDG Fuel Pressure Reads Below Min Value; 8/14/2017  
9/25/16
-
    - Apparent Cause Evaluation; EDG Speed Switch Failure, CR 02069073; 1/28/2016
21186; HVA/ACC-3B failure due to ground on condensing unit; 8/20/2017  
- AR 2035539; Maintenance Rule (a)(1) Action Plan; V18279 Check Valve for the 1A
-
Maintenance Hatch Door Seal Accumulator; 6/19/2015
22623; 1B2 EDG Needs Oil Added; 8/29/2017  
- AR 2074774; Maintenance Rule (a)(1) Action Plan; 4kV and 6.9kV, System 53;
-
6/21/2017
22743; U1 ACC-3 thermostat not responding; 8/29/2017  
- AR 2110122; Maintenance Rule (a)(1) Action Plan; Low Accumulator Pressure; Revision
-
1; 10/12/2017
24199; MFIV Oil Reservoir At The Low Level Mark; 9/10/2017  
- AR 2148252; Maintenance Rule (a)(1) Action Plan; V3217, SI Loop 1A2 Check Valve;
-
10/17/2016
24325; Unacceptable performance for post-hurricane accountability; 9/11/2017  
- AR 2151217; Maintenance Rule (a)(1) Action Plan; Main Generator System 53a;
-
2/2/2016
26606; 2B EDG Load Transient During Performance Of 2-OSP-59.01B; 9/25/17  
- AR 2213017; Maintenance Rule (a)(1) Action Plan; 2B Component Cooling Water;
-
Revision 1; 11/3/2017
27429; Fire Protection Program Implementation Cognitive Trend; 9/28/2017  
- AR 2218382; Maintenance Rule (a)(1) Action Plan; control Room Ventilation System;
-
Revision 1
29920; 2B EDG Fuel supply; 10/12/2017  
- EDG System; Design Basis Document DBD-EDG-1; Revision 10
-
- EDG System; Design Basis Document DBD-EDG-2; Revision 9
230410; Elevated contamination in room; 10/14/2017  
- Equipment Apparent Cause Evaluation; 1A EDG Abnormal Sounds and Indications After
-
Start; AR 02053060; 1/21/2016
230610; Level 1 Assessment - Fire Protection Program Implementation; 10/16/2017  
- NEESLX138-PR-01; NFPA 30 Code Compliance Independent Review; Revision 1
-
- Nuclear Safety Culture Monitoring Panel; 4Q17 Data; 1/11/2018
230758; OE-Industry White finding for EDG Diode Failure Catawba; 10/17/2017  
- Nuclear Safety Culture Sub-Committee; 3Q17 Data
-
- Nuclear Safety Culture Sub-Committee; 2Q17 Data
232779; U2 C AFW Flow Transmitters Isolated; 10/25/2017  
- PSL-ENG-SEMS-17-007; St. Lucie Unit 1 Hot Leg Injection Failure Modes and Effects
-
Analysis; Rev. 0; 9/25/2017
232782 1A MSL Rad Monitor Frequently Spiking Into Alarm. Inop. 10/25/17  
- Quality Assurance Topical Report FPL-1; Revision 21
-
- System Health Report, Unit 1 Auxiliary Feedwater System, Q2-2018
233080; Multiple CBCS Deficiencies Create Operator Burdens; 10/27/2017  
- System Health Report, Unit 2 Auxiliary Feedwater System, Q2-2018
-
- System Health Report; Unit 1 EDG; Q2-2018
233516; Work Request Cancelled w/o Any Work Performed on Active Leak;
- System Health Report; Unit 1 EDG; Q2-2018
10/29/2017  
- Unit 1 System 25b (Heating, Ventilation & Air Conditioning - Non-Risk significant )
-
System Health Report; 4/18/2018
233669; Recommended Actions From Previous AR 02110464 Not Addressed;
- Unit 2 System 25b (Heating, Ventilation & Air Conditioning - Non-Risk significant)
10/30/2017  
System Health Report; 4/18/2018
-
- Unit 1 System 18 (Instrument & Service Air) System Health Report; 4/18/2018
234317; 2-FSG-10, Safety Injection Tank Isolation - Rev 2; 11/2/2017  
- Unit 2 System 18 (Instrument & Service Air) System Health Report; 4/18/2018
-
2
235711; U1 ACC-3B low oil level; 11/10/2017  
-
236131; Tritium detected in catch basins; 11/14/2017  
-
237096; U1 HVA-3C compressor going into pump down; 11/20/2017  
-
238413; Part 21 Report, Fisher Information Notice 17-05; 11/30/2017  
-
238617; 1b AFW Pp THRST BRN Preload/Early Stage Wear - Contingency; 12/1/2017  
-
242181; Increased Flow Coming From 2B EDG OIL LEAK; 12/27/2017  
-
243677; Nuc. Assurance Escalation. L1: Inadequate use of GFCI protection; 1/9/2018  
 
-
243798; Water Leaking from Cell Jar Lids; 1/9/2018  
-
245101; 2D Instrument air compressor motor overload; 1/18/2018  
-
245821; Low Level In Reservoir; 1/23/2018  
-
246135; Inappropriate Use of MA Assignments for CAQ CRs; 1/24/2018  
-
249170; One-Hour Notification; 2/13/2018  
-
249174; Contamination in a clean area; 2/12/2018  
-
249292;1b AFW Pp Outboard Cover Guard Corroded; 02/13/2018  
-
249873; NRC evaluated drill 2018SAE not performed IAW drill scenario; 2/15/2018  
-
249999; Nuc. Assurance Escalation. L1: Metal shavings on plant equipment;
2/16/2018  
-
250930; PI&R Self Assessment; 2/22/2018  
-
250938; PI&R Self Assessment; 2/22/2018  
-
253212; Siren #1 failure; 3/8/2018  
-
253859; 1A EDG Failed Response Time Testing; 3/13/18  
-
254424; Alternate Source Supplying Load Light Will Not Illuminate; 3/15/2018  
-
254769; Higher than expected dose rates on refuel bridge; 3/19/2018  
-
255082; Inadequate commercial grade dedication resulted in Part 21; 3/20/2018  
-
256602; NRC Ident: Metal Shavings, Unit 1 Vital AC SUPS and 1C HPSI; 3/28/2018  
-
257037; Ris-26-13-1 Reading High Alarm; 03/30/2018  
-
257077; 2B2 EDG Engine Needs Oil Added; Unsafe To Do So Manually; 3/30/2018  
-
257159; Through wall leak on SW line reducer weld; 3/30/2018  
-
257515; Personnel contamination event; 4/2/2018  
-
257712; RM-26-12 failure causing 2-AOP-26.01 entry; 4/3/2018  
-
258467; MV-09-9 'A' AFW To 'A' S/G Failed To Control; 4/8/2018  
-
258467; Mv-09-9 'A' AFW To 'A' S/G Failed To Control; 4/8/2018  
-
258467; MV-09-9 'A' AFW To 'A' S/G Failed To Control; 4/8/2018  
-
259242; Level 1 Assessment of Part 21 Process; 4/12/2018  
-
259520; Metallic Debris on floor of U2 switchgear rooms; 4/18/2018  
-
263320; PI Processbook Unable to Calculate RCS Leak Rate; 5/9/2018  
-
264338; 2018 NRC PI&R Inspection EDG Mission Time; 5/15/2018  
-
Security-related CRs were reviewed during the inspection
Procedures  
-
1-GMM-80.41; Atwood & Morrill 12 Inch Swing Check Valve Maintenance; Revision 7  
-
1-OSP-63.13A; ESF - Staggered 36 Month Surveillance For SIAS/CIS/CSAS - Train A;
Revisions 32 & 33  
-
2-FSG-10; Safety Injection Tank Isolation; Revision 2  
-
2-GMM-03.02; Westinghouse 12 Inch Swing Check Valve Maintenance; Revision 2  
-
2-GMM-03.04; Westinghouse 3 Inch Swing Check Valve Maintenance; Revision 4  
-
ADM-17.32; Structures Monitoring Program; Revision 6  
-
EN-AA-203-1001; Operability Determinations / Functionality Assessments; Revision 29  
-
ER-AA-100-2002; Maintenance Rule Program Administration; Revision 6  
-
ER-AA-124; Check Valve Program, Revision 1  
-
NA-AA-200-1000; Employee Concerns Program; Revision 1  
-
PI-AA-100; Condition Assessment and Response; Revision 10  
-
PI-AA-100-1005; Root Cause Analysis; Revision 17  
-
PI-AA-100-1006; Common Cause Evaluation; Revision 13  
-
PI-AA-100-1007; Issue Investigation; Revision 20  
-
PI-AA-101; Assessment and Improvement Programs; Revision 24  
-
PI-AA-102-1002; Internal Operating Experience; Revision 8  
-
PI-AA-102-1003; Sharing Operating Experience With Nuclear Industry; Revision 12  
 
-
PI-AA-104-1000; Condition Reporting; Revision 17  
-
PI-AA-207; Trend Coding and Analysis; Revision 13  
-
PI-AA-207-1000; Station Self-Evaluation and Trending Analysis; Revision 8  
-
SY-AA-102-1000; Safeguards Information Program; Revision 15
Self-Assessments, Audits, and Trend Reports  
-
4Q17 PSL Self-Evaluation and Trending Analysis Report  
-
4Q17 PSL/Engineering Self-Evaluation and Trending Analysis Report  
-
4Q17 PSL/Maintenance Self-Evaluation and Trending Analysis Report  
-
4Q17 PSL/Operations Self-Evaluation and Trending Analysis Report  
-
4Q17 PSL/Radiation Protection Self-Evaluation and Trending Analysis Report  
-
4Q17 PSL/Security Self-Evaluation and Trending Analysis Report  
-
Pre-NRC Problem Identification & Resolution (PI&R) Inspection Assessment  
-
PSL 16-002 Radiation Protection and Radwaste Audit Report; 5/26/2016  
-
PSL 16-005 EP Audit Report; 8/10/2016  
-
PSL 16-006; Operations; 9/7/2016  
-
PSL 16-009 Chemistry Audit Report; 1/04/2017  
-
PSL 17-003 QA Programs Audit Report; /18/2017  
-
PSL 17-005; Engineering Audit; 6/30/2017  
-
PSL 17-007 Emergency Preparedness Audit Report; 8/10/2017  
-
PSL 17-010; Performance Improvement; 1/25/2018  
-
PSL 17-012; Time Sensitive Action Review; 12/21/2017
Work Orders  
-
276910-01  
-
276911-01  
-
284284
-
40374092  
-
40374094  
-
40398730  
-
40410089  
-
40411087  
-
40469413  
-
40471113  
-
40472171  
-
40477208  
-
40477338  
-
40490422  
-
40521769  
-
40538193  
-
40591898  
-
94141676  
-
94143832  
-
94156308  
-
94172111
Other  
-
Alternative Analysis Unit 2 DOST NFPA 30 Section 2348 Compliance AR 2151322-10;
9/25/16  
-
Apparent Cause Evaluation; EDG Speed Switch Failure, CR 02069073; 1/28/2016  
 
-
AR 2035539; Maintenance Rule (a)(1) Action Plan; V18279 Check Valve for the 1A
Maintenance Hatch Door Seal Accumulator; 6/19/2015  
-
AR 2074774; Maintenance Rule (a)(1) Action Plan; 4kV and 6.9kV, System 53;
6/21/2017  
-
AR 2110122; Maintenance Rule (a)(1) Action Plan; Low Accumulator Pressure; Revision
1; 10/12/2017  
-
AR 2148252; Maintenance Rule (a)(1) Action Plan; V3217, SI Loop 1A2 Check Valve;
10/17/2016  
-
AR 2151217; Maintenance Rule (a)(1) Action Plan; Main Generator System 53a;
2/2/2016  
-
AR 2213017; Maintenance Rule (a)(1) Action Plan; 2B Component Cooling Water;
Revision 1; 11/3/2017  
-
AR 2218382; Maintenance Rule (a)(1) Action Plan; control Room Ventilation System;
Revision 1  
-
EDG System; Design Basis Document DBD-EDG-1; Revision 10  
-
EDG System; Design Basis Document DBD-EDG-2; Revision 9  
-
Equipment Apparent Cause Evaluation; 1A EDG Abnormal Sounds and Indications After
Start; AR 02053060; 1/21/2016  
-
NEESLX138-PR-01; NFPA 30 Code Compliance Independent Review; Revision 1  
-
Nuclear Safety Culture Monitoring Panel; 4Q17 Data; 1/11/2018  
-
Nuclear Safety Culture Sub-Committee; 3Q17 Data  
-
Nuclear Safety Culture Sub-Committee; 2Q17 Data  
-
PSL-ENG-SEMS-17-007; St. Lucie Unit 1 Hot Leg Injection Failure Modes and Effects
Analysis; Rev. 0; 9/25/2017  
-
Quality Assurance Topical Report FPL-1; Revision 21  
-
System Health Report, Unit 1 Auxiliary Feedwater System, Q2-2018  
-
System Health Report, Unit 2 Auxiliary Feedwater System, Q2-2018  
-
System Health Report; Unit 1 EDG; Q2-2018  
-
System Health Report; Unit 1 EDG; Q2-2018  
-
Unit 1 System 25b (Heating, Ventilation & Air Conditioning - Non-Risk significant )
System Health Report; 4/18/2018  
-
Unit 2 System 25b (Heating, Ventilation & Air Conditioning - Non-Risk significant)
System Health Report; 4/18/2018  
-
Unit 1 System 18 (Instrument & Service Air) System Health Report; 4/18/2018  
-
Unit 2 System 18 (Instrument & Service Air) System Health Report; 4/18/2018
}}
}}

Latest revision as of 18:14, 5 January 2025

Nuclear Regulatory Commission Problem Identification and Resolution Inspection Report 05000335/2018010 and 05000389/2018010
ML18171A249
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 06/20/2018
From: Randy Musser
NRC/RGN-II/DRP/RPB3
To: Nazar M
Florida Power & Light Co
References
IR 2018010
Download: ML18171A249 (11)


Text

June 20, 2018

SUBJECT:

ST. LUCIE PLANT - NUCLEAR REGULATORY COMMISSION PROBLEM

IDENTIFICATION AND RESOLUTION INSPECTION REPORT

05000335/2018010 AND 05000389/2018010

Dear Mr. Nazar:

On May 25, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed a problem identification and resolution inspection at your St. Lucie Plant, Units 1 and 2. On that date, the NRC inspectors discussed the results of this inspection with Mr. Robert Coffey, Southern Regional Vice President, and other members of your staff. The results of this inspection are documented in the enclosed inspection report.

The NRC inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs. Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

The team also evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.

Based on the samples reviewed, the team determined that your staffs performance in each of these areas adequately supported nuclear safety.

Finally, the team reviewed the stations programs to establish and maintain a safety-conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs. Based on the teams observations and the results of these interviews, the team found no evidence of challenges to your organizations safety-conscious work environment.

Your employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

The NRC inspectors did not identify any finding or violation of more than minor significance. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Randall A. Musser, Chief

Reactor Projects Branch 3

Division of Reactor Projects

Docket Nos.: 50-335, 50-389 License Nos.: DPR-67, NPF-16

Enclosure:

IR 05000335/2018010 and 05000389/2018010

REGION II==

Docket Nos.:

50-335, 50-389

License Nos.:

DRP-67, NPF-16

Report Nos.:

05000335/2018010, 05000389/2018010

Enterprise Identifier: I-2018-010-0045

Licensee:

Florida Power & Light Company (FPL)

Facility:

St. Lucie Plant, Units 1 and 2

Location:

6501 South Ocean Drive Jensen Beach, FL 34957

Dates:

May 7 through May 25, 2018

Inspectors:

A. Wilson, Project Engineer, Team Leader L. Pressley, Senior Project Engineer S. Roberts, Resident Inspector J. Rotton, Senior Resident Inspector

Approved by:

Randall A. Musser, Chief Reactor Projects Branch 3 Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting a Problem Identification and Resolution Inspection at St. Lucie Plant, Units 1 and 2 in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings were identified.

INSPECTION SCOPE

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met, consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71152B - Problem Identification and Resolution

The inspectors performed a biennial assessment of the licensees corrective action program, use of operating experience, self-assessments and audits, and safety-conscious work environment. The assessment is documented below.

(1) Corrective Action Program Effectiveness: Problem Identification, Problem Prioritization and Evaluation, and Corrective Actions - The inspection team reviewed the stations corrective action program and the stations implementation of the program to evaluate its effectiveness in identifying, prioritizing, evaluating, and correcting problems, and to confirm that the station was complying with NRC regulations and licensee standards for corrective action programs.
(2) Operating Experience and Self-Assessments and Audits - The team evaluated the stations processes for use of industry and NRC operating experience information and the effectiveness of the stations audits and self-assessments.
(3) Safety Conscious Work Environment - The team reviewed the stations programs to establish and maintain a safety-conscious work environment, and interviewed station personnel to evaluate the effectiveness of these programs.

INSPECTION RESULTS

Corrective Action Program Effectiveness Observations 71152Problem Identification and Resolution Based on the samples reviewed, the team determined that the licensees corrective action program (CAP) complied with regulatory requirements and self-imposed standards. The licensees implementation of the CAP adequately supported nuclear safety.

Effectiveness of Problem Identification: The inspectors determined that the licensee was effective in identifying problems and entering them into the CAP and there was a low threshold for entering issues into the CAP. This conclusion was based on a review of the requirements for initiating Condition Reports (CRs) as described in licensee procedure PI-AA-104-1000, Condition Reporting, and managements expectation that employees were encouraged to initiate CRs for any reason. Additionally, site management was actively involved in the CAP and focused appropriate attention on significant plant issues.

Based on reviews and walkdowns of accessible portions of selected systems, the inspectors determined that deficiencies were being identified and placed in the CAP.

Effectiveness of Prioritization and Evaluation of Issues: Based on the review of CRs sampled by the inspection team during the onsite period, the inspectors concluded that problems were generally prioritized and evaluated in accordance with the CR significance determination guidance in procedure PI-AA-104-1000. The inspectors determined that in general, adequate consideration was given to system or component operability and associated plant risk.

The inspectors determined that plant personnel had conducted root cause and apparent cause analyses in compliance with the licensees CAP procedures and cause determinations were appropriate, and considered the significance of the issues being evaluated. A variety of formal causal-analysis techniques were used to evaluate CRs depending on the type and complexity of the issue consistent with the applicable cause evaluation procedures.

The inspection team identified one issue of concern regarding the failure to properly consider mission time of Emergency Diesel Generators (EDGs) in operability evaluations in accordance with Procedure EN-AA-203-1001, Operability Determinations / Functionality Assessments, Revision 29. This issue was entered into the licensees CAP as CR 2264338 and is documented as a minor performance deficiency in the section below.

Effectiveness of Corrective Actions: Based on a review of corrective action documents, interviews with licensee staff, and verification of completed corrective actions, the inspectors determined that overall, corrective actions were timely, commensurate with the safety significance of the issues, and effective, in that conditions adverse to quality were corrected.

For significant conditions adverse to quality, the corrective actions directly addressed the cause and effectively prevented recurrence. The team reviewed performance indicators, CRs, and effectiveness reviews, as applicable, to verify that the significant conditions adverse to quality had not recurred. Effectiveness reviews for corrective actions to prevent recurrence (CAPRs) were sufficient to ensure corrective actions were properly implemented and were effective.

Minor Performance Deficiency 71152Problem Identification and Resolution Minor Performance Deficiency: The station failed to properly consider mission time of EDGs in operability evaluations in accordance with Procedure EN-AA-203-1001. Specifically, as documented in several CRs, the conclusions provided within the operability analysis sections could not be supported without evaluating the conditions against the system mission time.

The inspectors reviewed CRs 2132695, 2132704, and 2132705, which were all initiated to document oil leaks on the EDGs. Each CR contained a statement that, there is no impact on the ability of the EDG to meet its mission time, under the operability notes.

The inspectors reviewed the EDG Design Basis Documents (DBD-EDG-1, -2) for the defined mission time and determined that an official mission time had not been established for the EDGs. The inspectors interviewed a sample of senior reactor operators and determined that the mission time used for operability determinations had been a loosely based time derived from EDG placards and day tanks and diesel oil storage tank capacities.

Procedure EN-AA-203-1001 governed operability determinations at St. Lucie Plant. Step 4.2.2.2 directed that the screener of a condition report shall perform the Operability/Functionality Review screening using guidance in Attachment 1. Step 6, Table C of Attachment 1 required the screener to evaluate that the condition did not impair completion of design mission time.

For issues that required immediate operability determinations, Step 4.3.6 directed the Shift Manager to prepare the Immediate Operability Determination using the guidance of 2, Immediate Operability Determination Guidelines. Attachment 2, Step 2 stated:

In order to be considered operable, a SSC must be capable of performing the specified safety functions of its design, within the required range of physical conditions, initiation times, and mission times assumed in the CLB. For operability determination purposes, the mission time was the duration of SSC operation that was credited in the design basis for the SSC to perform its specified safety function.

In addition, Attachment 2, Step 8, stated: If oil leakage is detected from either a pump bearing housing, a motor bearing housing, or a governor, then leakage rate and mission time must be addressed.

Contrary to the above, because a mission time had not been established in the EDG Design Basis Documents (DBD-EDG-1, -2) for the EDGs, the ability of the system to remain operable for the duration of its mission time had not been appropriately evaluated for several conditions associated with EDGs.

CR 2264338 was originated to address the issue. The licensee had initiated actions to establish an official EDG mission time within the Design Basis Documents and perform an extent of condition to determine if a mission time needed to be established for other plant systems.

Screening: The inspectors screened the issue in accordance with Inspection Manual Chapter 0612, Appendix B, Issue Screening, and determined that the performance deficiency did not meet the criteria in Block 3 to be a More-than-Minor issue. The inspectors determined that the CRs reviewed for this instance were minor in nature and therefore would unlikely change the outcome of the operability determinations of the examples reviewed. The inspectors did not identify a violation of regulatory requirements associated with this minor performance deficiency.

Operating Experience and Self-Assessments and Audits Observations 71152Problem Identification and Resolution Based on the samples reviewed, the team determined that stations processes for the use of industry and NRC operating experience information and for the performance of audits and self-assessments were effective and complied with all regulatory requirements and licensee standards. The implementation of these programs adequately supported nuclear safety.

Overall, the team concluded that operating experience was adequately evaluated for applicability and that appropriate actions were implemented to address lessons learned as needed. In general, the inspectors determined that the licensee was effective at performing self-assessments and audits to identify issues at a low level, properly evaluated those issues, and resolved them commensurate with their safety significance.

Safety Conscious Work Environment Observations 71152Problem Identification and Resolution Based on interviews with plant staff and reviews of the latest safety culture survey results to assess the safety-conscious work environment on site, the team found no evidence of challenges to safety-conscious work environment. Employees appeared willing to raise nuclear safety concerns through at least one of the several means available.

EXIT MEETINGS AND DEBRIEFS

The inspectors confirmed that proprietary information was controlled to protect from public disclosure. No proprietary information was documented in this report.

  • On May 25, 2018, the inspectors presented the problem identification and resolution inspection results to Mr. Robert Coffey, Southern Regional Vice-President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Condition Reports

-

1893969; Replace All 9 Bus Vent Covers on 1A UAT; 8/2/2013

-

20696; Unit 2 Manual Reactor Trip; 11/14/2013

-

20742; Found Degraded Relays During Extent of Condition; 11/15/2013

-

1937045; HCV-14-11A1 Seal Cooler Valve Failed Closed; 1/29/2014

-

1948469; V381 Over Thrust During Disk Pull Out; 3/15/2014

-

1951584; Degraded Contacts Prevented 2B EDG Breaker From Closing; 3/25/2014

-

1973521; LPM Channel 1 Below Minimum Threshold; 6/20/2014

-

2054489 'B' RPS CNTMT Press Bistable Trip & Pre-Trip Lights Inop; 06/16/2015

-

2077661; 2C ICW Pp Motor Tripped On Overcurrent; 9/30/2015

-

2083954; Indicator Stuck At The Top Of The Gauge; 10/23/2015

-

2084836; 2C AFW Pump Governor Oil Leak; 10/23/2015

-

2090225; Unauthorized entry into a High Radiation area; 5/3/2016

-

2095560; U1 Circ Water DFS Filter DF-21-1B1 High DP Condition; 12/5/2015

-

2108156; EDG 1A One Engine Fail To Start Alarm Locks In During Surv; 02/06/2016

-

2108868; 2016 CDBI Functionality of EER Sup Fan Discharge Dampers, GD-1/2;

2/9/2016

-

2109116; 2016 CDBI HVAC Action in 1-EOP-09; 2/10/2016

-

2109310; Hydrogen Purity Local Meter Not Indicating Correct Purity; 2/11/2016

-

2111358; Failure to verify adequacy of Unit 1 Electrical Equipment room ventilation

system; 04/11/2016

-

2112128; Reverse Flow & Backward Rotation Observed on HVS-5A/B

-

2114645; 10 CFR Part 21 issue for Masterpack NT & NW breakers; 1/18/2017

-

2117193; Failure to verify adequacy of Unit 1 Electrical Equipment room ventilation

system; 04/11/2016

-

25717; ACE to Address Green NCV on CAQ for EER Supply Fans; 7/14/2016

-

28716; Loose Parts Monitoring Alarm For Channel 4; 4/29/2016

-

29351; Control Room Shift Communicator failure on simulator; 5/2/2016

-

2131209; "A" EDG Conduit Covers Loose; 5/11/2016

-

2131211; "A" EDG Conduit Termination Pulled Loose; 5/11/2016

-

2131215; 1A EDG Set Instrument Tubing In Contact With Each Other; 5/11/2016

-

2131219; 1A1 EDG Machine Screw Found Out Of Place; 5/11/2016

-

2132695; Valve Gallery Cover On 1A2 EDG Leaking Oil; 5/18/2016

-

2132704; 1A1 EDG Turbocharger Flange Oil Leak; 5/18/2016

-

2132705; 1A1 EDG Camshaft Covers Leaking Oil; 5/18/2016

-

2133018; UNIT 2 2A2 EDG Fuel Pressure Low; 5/19/2016

-

2133422; 2B MSIV accumulator corrosion; 5/22/2016

-

2133504; 2D Instrument air compressor not loading; 5/23/2016

-

2133774; 2D Instrument air compressor trip on high cylinder temperature; 5/24/2016

-

2134435; NOS Finding - Radioactive material stored outdoors; 5/26/2016

-

2135100; 1A EDG MVAR Readings Off Normal; 5/31/2016

-

2135780; NRC EQ Inspection - Containment High Range Radiation Monitors; 6/2/2016

-

2136211; TR-1112 Failed Low Affecting DCS and A QSPDS; 6/6/2016

-

2136427; ROTORK Controls, Inc. and Electroswitch Part 21 issues; 6/7/2016

-

2137373; DCS Point 2CSFM 10:P8023a A.PNT; 6/10/2016

-

2140294; 2D Instrument air compressor trip during performance run; 6/24/2016

-

2140595; 1A EDG MVAR Swings; 6/27/2016

-

2143046; U2 RCS Zinc concentration dropped below threshold limit; 7/12/2016

-

2143242; Evaluation of U2 ACC-3C refrigeration migration issue; 7/12/201

-

2144201; Shortfall in observations of Radiological work practices; 7/17/2016

-

2144412; 1A Fire pump breaker,1-40209, 10 CFR Part issue; 7/18/2016

-

2144416; 2AB to 2B2 bus tie breaker, 2-40706, 10 CFR Part 21 issue; 7/18/2016

-

2145831; Condition of RABS unsat; 7/25/2016

-

2146175; U1 RCS Zinc concentration less than admin limit; 7/27/2016

-

2148252; V3217 Backleakage During Shutdown Cooling Flush; 8/6/16

-

2149500; Mv-09-11 Only Strokes Closed Intermittently; 8/12/2016

-

2150868; Work hours control violation; 8/18/2016

-

2151322; Inadequate Modification Of The Unit 2 DOST, EC274456; 8/22/2016

-

2151502; High Radiation Area and contamination area created due to RES; 8/23/2016

-

2152647; Instrument air system pressure degrading trend; 8/28/2016

-

2154938; All NRC ENS phone lines OOS; 9/9/2016

-

2155627; Untimely classification resulting in missed DEP-PI; 9/13/2016

-

2156690; Recovery plan for exercise and drill performance; 9/19/2016

-

2156817; DEP miss due to inaccurate state notification during SIMEVAL; 9/20/2016

-

2157214; 1B DC Bus Ground Locked In; 9/21/2016

-

2157980; Core Exit Thermocouple 16 Q-3, Continues To Drop Out Low; 09/25/2016

-

2158314; U1 CCW Tritium greater than MDA; 9/27/2016

-

2160390; 1B EDG Room Floor Drain Backing Up; 10/5/2016

-

2165042; Foamy oil in U1 ACC-3C, control room air conditioner; 10/25/2016

-

2165690; 1A EDG MVAR Swings During Adjustments; 10/27/2016

-

2166772; Industry OE - Harris NOUE (LOOP); 11/1/2016

-

2166950; EDG LOOP Response Time Safeguards Acceptance Criteria; 11/1/2016

-

2167267; Industry OE - Farley Alert due to toxic gas; 11/3/2016

-

2168328; Leakage Past V09248; 11/9/2016

-

2168775; Industry OE - Dresden U3 Alert-ICES Report# 323383; 11/11/2016

-

2168864; WO: 40499100-01 Inadvertently Closed In EWP; 11/11/2016

-

2174203; Loose Parts Monitor Alarming; 12/12/2016

-

2175061; EDG Starting Air Leakage Test Margin Recovery; 12/15/2016

-

2175530; During Sl-1-27, V09280 Was Worked And PMT Was Not Completed;

2/15/2016

-

2175641; L-31, Boron Concentration Low Channel 1 Alarming; 12/17/2016

-

2176118; Inappropriate long term storage of radioactive material; 12/21/2016

-

2179806; 2D Instrument air compressor excessive cycling; 1/14/2017

-

2181204; Declining RCA Radiation Worker observation trend; 1/23/2017

-

2183774; ALARA near miss due to inadequate scaffold; 2/4/2017

-

2184494; PSL Siren S-70 test failure; 2/8/2017

-

2185542; Waste processing challenges due to U1 AWST Activity; 2/14/2017

-

2186438; HVA/ACC-3B Freon leak; 2/17/2017

-

2187133; 2B EDG Jacket Water Temp Low During Safeguards; 2/21/17

-

2187169; OE regarding a loss of instrument air (NRC IN 2016-05); 2/22/2017

-

2187670; AFW PP 1C-PP OTBD Brg Wear-Increased Particle Concentration; 2/23/2017

-

2188004; Personnel contamination event / PCE #17-013; 2/25/2017

-

2188010; The Wrong Pc Level Oil Was Used In The 1c Auxiliary FW Pump; 2/25/2017

-

2188020; SE-07-5F Solenoid Valve PEN P-51, Field Wires Damaged; 3/1/2017

-

2188171; Personnel contamination event / PCE #17-015; 2/26/2017

-

2188184; EDG Fuel Oil Cross-Connect Surveillance Conundrum; 2/27/17

-

2188751; Engineered Safeguard Logic Cabinet Sa Volt Meter Failed; 03/01/2017

-

2189467; 2A Instrument air dryer blowing down continuously; 3/4/2017

-

2189538; 1C Instrument air compressor low oil level; 3/5/2017

-

2190852; 1C Instrument air compressor excessive oil consumption; 3/11/2017

-

2190895; 20 Gallons Of Oil Added To 2A1 Engine On 2A EDG; 3/11/2017

-

2190896; 12 Gallons Of Oil Added To 2A2 Engine On 2A EDG; 3/11/2017

-

2192588; A Feedwater Header Mfiv,HCV-09-1,Hydraulic Actuator Issue; 3/21/2017

-

2193112; 2B2 RCP Lower Guide BRG Temp Inconsistent Output; 3/22/2017

-

2193490; 1C AFW Pp OTBD Oil Reservoir Drain/Flush Before Next Run; 3/24/2017

-

2193884; 1C Instrument air compressor oil leak; 3/25/2017

-

2194614; 1D Instrument air compressor low oil level; 3/29/2017

-

202422; HVA/ACC-3A Low Freon level while running; 4/30/2017

-

203125; Ladder laying across contaminated area boundary; 5/3/2017

-

203233; Request Conditional Release Of R&O 150 Oil For 2B EDG; 5/4/2017

-

204967; Industry OE - LaSalle Anchor Darling Part 21; 5/15/2017

-

205200; Unexpected Loss of the 2A3 4160V Safety Bus; 5/16/2017

-

205687; U1 CCW shows signs of Tritium activity; 5/17/2017

-

205761; 2A2 EDG Tubing Found Degraded; 5/18/2017

-

206260; HCV-09-2B Oil Leak; 5/21/2017

-

206286; 2A1 EDG Water Immersion Heater Tripping; 5/21/2017

-

207340; Level 1 Assessment - Trending Program at PSL; 5/26/2017

-

208096; Unit 1 TSC plant computer room air conditioning not cooling; 5/31/2017

23692; Incomplete actions from Hurricane Matthew assessment; 9/6/2017

-

210364; HVA 3A trip on motor temperature overload; 6/14/2017

-

212311; MCC AC-DC starter mechanical interlock reliability review; 6/26/2017

-

217392; Engineering to perform OE review Robinson Plane OE 241354; 7/27/2017

-

217631; U1 Hot Leg Injection Procedures; 7/29/2017

-

219154; HCV-09-2B Reservoir Oil Level Low In Spec Not An Active Leak; 8/8/2017

-

20259; 2A1 EDG Fuel Pressure Reads Below Min Value; 8/14/2017

-

21186; HVA/ACC-3B failure due to ground on condensing unit; 8/20/2017

-

22623; 1B2 EDG Needs Oil Added; 8/29/2017

-

22743; U1 ACC-3 thermostat not responding; 8/29/2017

-

24199; MFIV Oil Reservoir At The Low Level Mark; 9/10/2017

-

24325; Unacceptable performance for post-hurricane accountability; 9/11/2017

-

26606; 2B EDG Load Transient During Performance Of 2-OSP-59.01B; 9/25/17

-

27429; Fire Protection Program Implementation Cognitive Trend; 9/28/2017

-

29920; 2B EDG Fuel supply; 10/12/2017

-

230410; Elevated contamination in room; 10/14/2017

-

230610; Level 1 Assessment - Fire Protection Program Implementation; 10/16/2017

-

230758; OE-Industry White finding for EDG Diode Failure Catawba; 10/17/2017

-

232779; U2 C AFW Flow Transmitters Isolated; 10/25/2017

-

232782 1A MSL Rad Monitor Frequently Spiking Into Alarm. Inop. 10/25/17

-

233080; Multiple CBCS Deficiencies Create Operator Burdens; 10/27/2017

-

233516; Work Request Cancelled w/o Any Work Performed on Active Leak;

10/29/2017

-

233669; Recommended Actions From Previous AR 02110464 Not Addressed;

10/30/2017

-

234317; 2-FSG-10, Safety Injection Tank Isolation - Rev 2; 11/2/2017

-

235711; U1 ACC-3B low oil level; 11/10/2017

-

236131; Tritium detected in catch basins; 11/14/2017

-

237096; U1 HVA-3C compressor going into pump down; 11/20/2017

-

238413; Part 21 Report, Fisher Information Notice 17-05; 11/30/2017

-

238617; 1b AFW Pp THRST BRN Preload/Early Stage Wear - Contingency; 12/1/2017

-

242181; Increased Flow Coming From 2B EDG OIL LEAK; 12/27/2017

-

243677; Nuc. Assurance Escalation. L1: Inadequate use of GFCI protection; 1/9/2018

-

243798; Water Leaking from Cell Jar Lids; 1/9/2018

-

245101; 2D Instrument air compressor motor overload; 1/18/2018

-

245821; Low Level In Reservoir; 1/23/2018

-

246135; Inappropriate Use of MA Assignments for CAQ CRs; 1/24/2018

-

249170; One-Hour Notification; 2/13/2018

-

249174; Contamination in a clean area; 2/12/2018

-

249292;1b AFW Pp Outboard Cover Guard Corroded; 02/13/2018

-

249873; NRC evaluated drill 2018SAE not performed IAW drill scenario; 2/15/2018

-

249999; Nuc. Assurance Escalation. L1: Metal shavings on plant equipment;

2/16/2018

-

250930; PI&R Self Assessment; 2/22/2018

-

250938; PI&R Self Assessment; 2/22/2018

-

253212; Siren #1 failure; 3/8/2018

-

253859; 1A EDG Failed Response Time Testing; 3/13/18

-

254424; Alternate Source Supplying Load Light Will Not Illuminate; 3/15/2018

-

254769; Higher than expected dose rates on refuel bridge; 3/19/2018

-

255082; Inadequate commercial grade dedication resulted in Part 21; 3/20/2018

-

256602; NRC Ident: Metal Shavings, Unit 1 Vital AC SUPS and 1C HPSI; 3/28/2018

-

257037; Ris-26-13-1 Reading High Alarm; 03/30/2018

-

257077; 2B2 EDG Engine Needs Oil Added; Unsafe To Do So Manually; 3/30/2018

-

257159; Through wall leak on SW line reducer weld; 3/30/2018

-

257515; Personnel contamination event; 4/2/2018

-

257712; RM-26-12 failure causing 2-AOP-26.01 entry; 4/3/2018

-

258467; MV-09-9 'A' AFW To 'A' S/G Failed To Control; 4/8/2018

-

258467; Mv-09-9 'A' AFW To 'A' S/G Failed To Control; 4/8/2018

-

258467; MV-09-9 'A' AFW To 'A' S/G Failed To Control; 4/8/2018

-

259242; Level 1 Assessment of Part 21 Process; 4/12/2018

-

259520; Metallic Debris on floor of U2 switchgear rooms; 4/18/2018

-

263320; PI Processbook Unable to Calculate RCS Leak Rate; 5/9/2018

-

264338; 2018 NRC PI&R Inspection EDG Mission Time; 5/15/2018

-

Security-related CRs were reviewed during the inspection

Procedures

-

1-GMM-80.41; Atwood & Morrill 12 Inch Swing Check Valve Maintenance; Revision 7

-

1-OSP-63.13A; ESF - Staggered 36 Month Surveillance For SIAS/CIS/CSAS - Train A;

Revisions 32 & 33

-

2-FSG-10; Safety Injection Tank Isolation; Revision 2

-

2-GMM-03.02; Westinghouse 12 Inch Swing Check Valve Maintenance; Revision 2

-

2-GMM-03.04; Westinghouse 3 Inch Swing Check Valve Maintenance; Revision 4

-

ADM-17.32; Structures Monitoring Program; Revision 6

-

EN-AA-203-1001; Operability Determinations / Functionality Assessments; Revision 29

-

ER-AA-100-2002; Maintenance Rule Program Administration; Revision 6

-

ER-AA-124; Check Valve Program, Revision 1

-

NA-AA-200-1000; Employee Concerns Program; Revision 1

-

PI-AA-100; Condition Assessment and Response; Revision 10

-

PI-AA-100-1005; Root Cause Analysis; Revision 17

-

PI-AA-100-1006; Common Cause Evaluation; Revision 13

-

PI-AA-100-1007; Issue Investigation; Revision 20

-

PI-AA-101; Assessment and Improvement Programs; Revision 24

-

PI-AA-102-1002; Internal Operating Experience; Revision 8

-

PI-AA-102-1003; Sharing Operating Experience With Nuclear Industry; Revision 12

-

PI-AA-104-1000; Condition Reporting; Revision 17

-

PI-AA-207; Trend Coding and Analysis; Revision 13

-

PI-AA-207-1000; Station Self-Evaluation and Trending Analysis; Revision 8

-

SY-AA-102-1000; Safeguards Information Program; Revision 15

Self-Assessments, Audits, and Trend Reports

-

4Q17 PSL Self-Evaluation and Trending Analysis Report

-

4Q17 PSL/Engineering Self-Evaluation and Trending Analysis Report

-

4Q17 PSL/Maintenance Self-Evaluation and Trending Analysis Report

-

4Q17 PSL/Operations Self-Evaluation and Trending Analysis Report

-

4Q17 PSL/Radiation Protection Self-Evaluation and Trending Analysis Report

-

4Q17 PSL/Security Self-Evaluation and Trending Analysis Report

-

Pre-NRC Problem Identification & Resolution (PI&R) Inspection Assessment

-

PSL 16-002 Radiation Protection and Radwaste Audit Report; 5/26/2016

-

PSL 16-005 EP Audit Report; 8/10/2016

-

PSL 16-006; Operations; 9/7/2016

-

PSL 16-009 Chemistry Audit Report; 1/04/2017

-

PSL 17-003 QA Programs Audit Report; /18/2017

-

PSL 17-005; Engineering Audit; 6/30/2017

-

PSL 17-007 Emergency Preparedness Audit Report; 8/10/2017

-

PSL 17-010; Performance Improvement; 1/25/2018

-

PSL 17-012; Time Sensitive Action Review; 12/21/2017

Work Orders

-

276910-01

-

276911-01

-

284284

-

40374092

-

40374094

-

40398730

-

40410089

-

40411087

-

40469413

-

40471113

-

40472171

-

40477208

-

40477338

-

40490422

-

40521769

-

40538193

-

40591898

-

94141676

-

94143832

-

94156308

-

94172111

Other

-

Alternative Analysis Unit 2 DOST NFPA 30 Section 2348 Compliance AR 2151322-10;

9/25/16

-

Apparent Cause Evaluation; EDG Speed Switch Failure, CR 02069073; 1/28/2016

-

AR 2035539; Maintenance Rule (a)(1) Action Plan; V18279 Check Valve for the 1A

Maintenance Hatch Door Seal Accumulator; 6/19/2015

-

AR 2074774; Maintenance Rule (a)(1) Action Plan; 4kV and 6.9kV, System 53;

6/21/2017

-

AR 2110122; Maintenance Rule (a)(1) Action Plan; Low Accumulator Pressure; Revision

1; 10/12/2017

-

AR 2148252; Maintenance Rule (a)(1) Action Plan; V3217, SI Loop 1A2 Check Valve;

10/17/2016

-

AR 2151217; Maintenance Rule (a)(1) Action Plan; Main Generator System 53a;

2/2/2016

-

AR 2213017; Maintenance Rule (a)(1) Action Plan; 2B Component Cooling Water;

Revision 1; 11/3/2017

-

AR 2218382; Maintenance Rule (a)(1) Action Plan; control Room Ventilation System;

Revision 1

-

EDG System; Design Basis Document DBD-EDG-1; Revision 10

-

EDG System; Design Basis Document DBD-EDG-2; Revision 9

-

Equipment Apparent Cause Evaluation; 1A EDG Abnormal Sounds and Indications After

Start; AR 02053060; 1/21/2016

-

NEESLX138-PR-01; NFPA 30 Code Compliance Independent Review; Revision 1

-

Nuclear Safety Culture Monitoring Panel; 4Q17 Data; 1/11/2018

-

Nuclear Safety Culture Sub-Committee; 3Q17 Data

-

Nuclear Safety Culture Sub-Committee; 2Q17 Data

-

PSL-ENG-SEMS-17-007; St. Lucie Unit 1 Hot Leg Injection Failure Modes and Effects

Analysis; Rev. 0; 9/25/2017

-

Quality Assurance Topical Report FPL-1; Revision 21

-

System Health Report, Unit 1 Auxiliary Feedwater System, Q2-2018

-

System Health Report, Unit 2 Auxiliary Feedwater System, Q2-2018

-

System Health Report; Unit 1 EDG; Q2-2018

-

System Health Report; Unit 1 EDG; Q2-2018

-

Unit 1 System 25b (Heating, Ventilation & Air Conditioning - Non-Risk significant )

System Health Report; 4/18/2018

-

Unit 2 System 25b (Heating, Ventilation & Air Conditioning - Non-Risk significant)

System Health Report; 4/18/2018

-

Unit 1 System 18 (Instrument & Service Air) System Health Report; 4/18/2018

-

Unit 2 System 18 (Instrument & Service Air) System Health Report; 4/18/2018