IR 05000313/2018004: Difference between revisions
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{{#Wiki_filter: | {{#Wiki_filter:January 23, 2019 | ||
==SUBJECT:== | ==SUBJECT:== | ||
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Sincerely, | Sincerely, | ||
/RA/ | /RA/ | ||
Neil OKeefe, Chief Project Branch D Division of Reactor Projects Docket Nos. 50-313 and 50-368 License Nos. DPR-51 and NPF-6 Enclosure: | |||
Neil OKeefe, Chief Project Branch D Division of Reactor Projects | |||
Docket Nos. 50-313 and 50-368 License Nos. DPR-51 and NPF-6 | |||
Enclosure: | |||
Inspection Report 05000313/2018004 and 05000368/2018004 w/Attachment: | Inspection Report 05000313/2018004 and 05000368/2018004 w/Attachment: | ||
Documents Reviewed | Documents Reviewed | ||
U.S. NUCLEAR REGULATORY COMMISSION | Enclosure U.S. NUCLEAR REGULATORY COMMISSION | ||
==Inspection Report== | ==Inspection Report== | ||
Docket Number(s): 05000313, 05000368 License Number(s): DPR-51, NPF-6 Report Number(s): 05000313/2018004, 05000368/2018004 Enterprise Identifier: I-2018-004-0005 Licensee: Entergy Operations, Inc. | Docket Number(s): | ||
05000313, 05000368 | |||
License Number(s): | |||
DPR-51, NPF-6 | |||
Report Number(s): | |||
05000313/2018004, 05000368/2018004 | |||
Enterprise Identifier: I-2018-004-0005 | |||
Licensee: | |||
Entergy Operations, Inc. | |||
Facility: | |||
Arkansas Nuclear One, Units 1 and 2 | |||
Location: | |||
Russellville, Arkansas | |||
Inspection Dates: | |||
October 1, 2018 to December 31, 2018 | |||
Inspectors: | |||
C. Henderson, Senior Resident Inspector | |||
M. Tobin, Resident Inspector | |||
T. Sullivan, Resident Inspector | |||
R. Bywater, Project Engineer | |||
J. Dixon, Senior Project Engineer | |||
S. Hedger, Emergency Preparedness Inspector | |||
Approved By: | |||
Neil OKeefe | |||
Branch Chief | |||
Division of Reactor Projects | |||
=SUMMARY= | =SUMMARY= | ||
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Arkansas Nuclear One, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A self-revealed violation and additional items are summarized in the tables below. | The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Arkansas Nuclear One, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A self-revealed violation and additional items are summarized in the tables below. | ||
List of Findings and Violations Failure to Fully Implement Vendor Manual Recommended Preventive Maintenance Cornerstone | ===List of Findings and Violations=== | ||
Failure to Fully Implement Vendor Manual Recommended Preventive Maintenance Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000368/2018004-01 Closed None 71152 - | |||
Problem Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment. | |||
Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches because only some electrical contacts were being cleaned. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing. | Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches because only some electrical contacts were being cleaned. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing. | ||
Additional Tracking Items Type | ===Additional Tracking Items=== | ||
Type Issue number Title Inspection Procedure Status LER 0500313/2016-003-01 | |||
Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1 71153 Closed LER 0500368/2017-001-00 Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions 71153 Closed LER 05000313/2018-002-01 Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld 71153 Closed | |||
=PLANT STATUS= | =PLANT STATUS= | ||
Unit 1 began the inspection period at full power. On November 29, 2018, power was lowered to 85 percent to perform main turbine valve testing and was returned to full power. | |||
On December 18, 2018, Unit 1 had an automatic reactor trip from 100 percent power after the loss of power to non-vital 4160 volt bus A1. On December 21, 2018, Unit 1 commenced a reactor startup and the reactor was made critical. The unit was returned to rated thermal power on December 23, 2018. | On December 18, 2018, Unit 1 had an automatic reactor trip from 100 percent power after the loss of power to non-vital 4160 volt bus A1. On December 21, 2018, Unit 1 commenced a reactor startup and the reactor was made critical. The unit was returned to rated thermal power on December 23, 2018. | ||
Unit 2 began the inspection period in shutdown for Refueling Outage 2R26, which started on September 29, 2018. On November 19, 2018, Unit 2 commenced a reactor startup and the reactor was made critical. The unit was returned to full power on November 24, | Unit 2 began the inspection period in shutdown for Refueling Outage 2R26, which started on September 29, 2018. On November 19, 2018, Unit 2 commenced a reactor startup and the reactor was made critical. The unit was returned to full power on November 24, | ||
==INSPECTION SCOPES== | ==INSPECTION SCOPES== | ||
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==REACTOR SAFETY== | ==REACTOR SAFETY== | ||
===71111.04Equipment Alignment Partial Walkdown=== | |||
===71111.04Equipment Alignment Partial Walkdown === | |||
{{IP sample|IP=IP 71111.04|count=5}} | {{IP sample|IP=IP 71111.04|count=5}} | ||
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains: | The inspectors evaluated system configurations during partial walkdowns of the following systems/trains: | ||
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: (3) Unit 1 train A high pressure injection system on November 21, 2018 | : (3) Unit 1 train A high pressure injection system on November 21, 2018 | ||
: (4) Unit 1 and Unit 2 quality condensate storage tank on November 28, 2018 | : (4) Unit 1 and Unit 2 quality condensate storage tank on November 28, 2018 | ||
: (5) Unit 2 train A plant protective system on December 31, 2018 | : (5) Unit 2 train A plant protective system on December 31, 2018 | ||
===71111.05AQFire Protection Annual/Quarterly Quarterly Inspection === | ===71111.05AQFire Protection Annual/Quarterly Quarterly Inspection=== | ||
{{IP sample|IP=IP 71111.05|count=6}} | {{IP sample|IP=IP 71111.05|count=6}} | ||
The inspectors evaluated fire protection program implementation in the following selected areas: | The inspectors evaluated fire protection program implementation in the following selected areas: | ||
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: (4) Unit 2 train A 2B53 switchgear room, Fire Area B, Zone 2091-BB, on November 22, 2018 | : (4) Unit 2 train A 2B53 switchgear room, Fire Area B, Zone 2091-BB, on November 22, 2018 | ||
: (5) Unit 1 north emergency diesel generator room, Fire Area D, Zone 86-G, on November 27, 2018 | : (5) Unit 1 north emergency diesel generator room, Fire Area D, Zone 86-G, on November 27, 2018 | ||
: (6) Unit 1 east (B) decay heat removal pump room, Fire Area A, Zone 10-EE, on November 28, 2018 | : (6) Unit 1 east (B) decay heat removal pump room, Fire Area A, Zone 10-EE, on November 28, 2018 | ||
===71111.07Heat Sink Performance Heat Sink === | ===71111.07Heat Sink Performance Heat Sink=== | ||
{{IP sample|IP=IP 71111.07|count=1}} | {{IP sample|IP=IP 71111.07|count=1}} | ||
The inspectors evaluated Unit 2 reactor building containment coolers 2VCC-2A/B/C/D performance on December 17, 2018. | The inspectors evaluated Unit 2 reactor building containment coolers 2VCC-2A/B/C/D performance on December 17, 2018. | ||
===71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification === | ===71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification=== | ||
{{IP sample|IP=IP 71111.11|count=1}} | {{IP sample|IP=IP 71111.11|count=1}} | ||
The inspectors observed and evaluated Unit 1 licensed operator requalification scenario on November 27, 2018. | The inspectors observed and evaluated Unit 1 licensed operator requalification scenario on November 27, 2018. | ||
Operator Performance (2 Samples)=== | ===Operator Performance (2 Samples)=== | ||
The inspectors observed and evaluated: | The inspectors observed and evaluated: | ||
: (1) Unit 2 reactor plant startup from Refueling Outage 2R26 on November 19, 2018 | |||
: (2) Unit 1 turbine stop valve testing on November 29, 2018 | |||
===71111.12Maintenance Effectiveness Routine Maintenance Effectiveness=== | |||
===71111.12Maintenance Effectiveness Routine Maintenance Effectiveness === | |||
{{IP sample|IP=IP 71111.12|count=1}} | {{IP sample|IP=IP 71111.12|count=1}} | ||
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety-significant functions: | The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety-significant functions: | ||
: (1) Unit 1 and Unit 2 50.65(a)(3) periodic evaluation on December 10, 2018 | : (1) Unit 1 and Unit 2 50.65(a)(3) periodic evaluation on December 10, 2018 | ||
===following equipment performance issues: | ===Quality Control (1 Sample)=== | ||
: (1) Unit 2 control element assembly CEA-5 capacitor replacement on December 10, 2018 | The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues: | ||
: (1) Unit 2 control element assembly CEA-5 capacitor replacement on December 10, 2018 | |||
===71111.13Maintenance Risk Assessments and Emergent Work Control === | ===71111.13Maintenance Risk Assessments and Emergent Work Control=== | ||
{{IP sample|IP=IP 71111.13|count=4}} | {{IP sample|IP=IP 71111.13|count=4}} | ||
The inspectors evaluated the risk assessments for the following planned and emergent work activities: | The inspectors evaluated the risk assessments for the following planned and emergent work activities: | ||
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: (2) Unit 2 plant protective system maintenance activities on October 31, 2018 | : (2) Unit 2 plant protective system maintenance activities on October 31, 2018 | ||
: (3) Unit 1 and Unit 2 stator heavy lift from onsite storage area to the barge on November 13, 2018 | : (3) Unit 1 and Unit 2 stator heavy lift from onsite storage area to the barge on November 13, 2018 | ||
: (4) Unit 1 emergent work for the loss of the train A non-vital 4160 volt bus A1 troubleshooting and repair on December 18, 2018 | : (4) Unit 1 emergent work for the loss of the train A non-vital 4160 volt bus A1 troubleshooting and repair on December 18, 2018 | ||
===71111.15Operability Determinations and Functionality Assessments === | ===71111.15Operability Determinations and Functionality Assessments=== | ||
{{IP sample|IP=IP 71111.15|count=3}} | {{IP sample|IP=IP 71111.15|count=3}} | ||
The inspectors evaluated the following operability determinations and functionality assessments: | The inspectors evaluated the following operability determinations and functionality assessments: | ||
: (1) Unit 2 reactor coolant system thermal sleeves operability assessment on November 2, 2018 | : (1) Unit 2 reactor coolant system thermal sleeves operability assessment on November 2, 2018 | ||
: (2) Unit 2 reactor vessel monitoring level system detector (RadCal) operability assessment on November 26, 2018 | : (2) Unit 2 reactor vessel monitoring level system detector (RadCal) operability assessment on November 26, 2018 | ||
: (3) Unit 1 sodium hydroxide spray additive system tank pitting below minimum wall thickness operability assessment on December 12, 2018 | : (3) Unit 1 sodium hydroxide spray additive system tank pitting below minimum wall thickness operability assessment on December 12, 2018 | ||
===71111.18Plant Modifications === | ===71111.18Plant Modifications=== | ||
{{IP sample|IP=IP 71111.18|count=2}} | {{IP sample|IP=IP 71111.18|count=2}} | ||
The inspectors evaluated the following permanent modifications: | The inspectors evaluated the following permanent modifications: | ||
: (1) Unit 2 control element assembly upper gripper coil stack replacements on October 26, 2018 | : (1) Unit 2 control element assembly upper gripper coil stack replacements on October 26, 2018 | ||
: (2) Unit 2 removal of timing uncertainty from the control element assembly drop time test on December 31, 2018 | : (2) Unit 2 removal of timing uncertainty from the control element assembly drop time test on December 31, 2018 | ||
===71111.19Post Maintenance Testing === | ===71111.19Post Maintenance Testing=== | ||
{{IP sample|IP=IP 71111.19|count=7}} | {{IP sample|IP=IP 71111.19|count=7}} | ||
The inspectors evaluated the following post-maintenance tests: | The inspectors evaluated the following post-maintenance tests: | ||
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: (5) Unit 2 check valve 2SI-14A inspection due to valve chattering on November 27, 2018 | : (5) Unit 2 check valve 2SI-14A inspection due to valve chattering on November 27, 2018 | ||
: (6) Unit 1 main feedwater block isolation valves repair on December 18, 2018 | : (6) Unit 1 main feedwater block isolation valves repair on December 18, 2018 | ||
: (7) Unit 2 restoration of lifted electrical leads during integrated safeguards testing on December 31, 2018 | : (7) Unit 2 restoration of lifted electrical leads during integrated safeguards testing on December 31, 2018 | ||
===71111.20Refueling and Other Outage Activities === | ===71111.20Refueling and Other Outage Activities=== | ||
{{IP sample|IP=IP 71111.20|count=2}} | {{IP sample|IP=IP 71111.20|count=2}} | ||
: (1) The inspectors evaluated Unit 2 Refueling Outage 2R26 activities from September 29 to November 2, 2018. | : (1) The inspectors evaluated Unit 2 Refueling Outage 2R26 activities from September 29 to November 2, 2018. | ||
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===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests: | ===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests: | ||
Routine === | Routine=== | ||
{{IP sample|IP=IP 71111.22|count=6}} | {{IP sample|IP=IP 71111.22|count=6}} | ||
: (1) Unit 2 reactor vessel foreign object search and retrieval on October 23, 2018 | : (1) Unit 2 reactor vessel foreign object search and retrieval on October 23, 2018 | ||
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: (4) Unit 2 as-found local leak-rate test for valve 2CV-5255-1 on November 16, 2018 | : (4) Unit 2 as-found local leak-rate test for valve 2CV-5255-1 on November 16, 2018 | ||
: (5) Unit 2 integrated safety system testing on November 16, 2018 | : (5) Unit 2 integrated safety system testing on November 16, 2018 | ||
: (6) Unit 2 emergency feedwater check valves 2EFW-28, 29, 30, and 31, on December 14, 2018 | : (6) Unit 2 emergency feedwater check valves 2EFW-28, 29, 30, and 31, on December 14, 2018 | ||
===71114.04Emergency Action Level and Emergency Plan Changes === | ===71114.04Emergency Action Level and Emergency Plan Changes=== | ||
{{IP sample|IP=IP 71114.04|count=1}} | {{IP sample|IP=IP 71114.04|count=1}} | ||
The licensee submitted a summary of Emergency Action Level classification procedure changes (Revision 57) to the NRC on October 4, 2018. The inspector conducted an in-office review of the changes from December 4, 2018, to December 14, 2018. This evaluation does not constitute NRC approval. | The licensee submitted a summary of Emergency Action Level classification procedure changes (Revision 57) to the NRC on October 4, 2018. The inspector conducted an in-office review of the changes from December 4, 2018, to December 14, 2018. This evaluation does not constitute NRC approval. | ||
==OTHER ACTIVITIES - BASELINE== | ==OTHER ACTIVITIES - BASELINE== | ||
===71151Performance Indicator Verification=== | |||
===71151Performance Indicator Verification === | |||
{{IP sample|IP=IP 71151|count=4}} | {{IP sample|IP=IP 71151|count=4}} | ||
The inspectors verified licensee performance indicators submittals listed below: | The inspectors verified licensee performance indicators submittals listed below: | ||
: (1) MS09: Unit 1 and Unit 2 Residual Heat Removal Systems (10/01/2017-09/30/2018) | : (1) MS09: Unit 1 and Unit 2 Residual Heat Removal Systems (10/01/2017-09/30/2018) | ||
: (2) MS10: Unit 1 and Unit 2 Cooling Water Support Systems (10/01/2017-09/30/2018) | : (2) MS10: Unit 1 and Unit 2 Cooling Water Support Systems (10/01/2017-09/30/2018) | ||
===71152Problem Identification and Resolution Semiannual Trend Review === | ===71152Problem Identification and Resolution Semiannual Trend Review=== | ||
{{IP sample|IP=IP 71152|count=2}} | {{IP sample|IP=IP 71152|count=2}} | ||
The inspectors reviewed the licensees corrective action program for trends that might be indicative of more significant safety issues: | The inspectors reviewed the licensees corrective action program for trends that might be indicative of more significant safety issues: | ||
: (1) Procedural quality involving the adequacy of surveillance testing acceptance criteria and testing methodology | : (1) Procedural quality involving the adequacy of surveillance testing acceptance criteria and testing methodology | ||
: (2) Common cause analysis of the ANO Unit 1 Refueling Outage 1R27 human performance issues, Condition Report CR-ANO-C-2018-02728 | : (2) Common cause analysis of the ANO Unit 1 Refueling Outage 1R27 human performance issues, Condition Report CR-ANO-C-2018-02728 | ||
===related to the following issues: | ===Annual Follow-up of Selected Issues (1 Sample)=== | ||
: (1) Unit 2 failure of train A safety-related 4160 volt breaker 2A-303 to automatically close and service water pump B to start during surveillance testing on December 17, 2018 | The inspectors reviewed the licensees implementation of its corrective action program related to the following issues: | ||
: (1) Unit 2 failure of train A safety-related 4160 volt breaker 2A-303 to automatically close and service water pump B to start during surveillance testing on December 17, 2018 | |||
===71153Follow-up of Events and Notices of Enforcement Discretion Events === | ===71153Follow-up of Events and Notices of Enforcement Discretion Events=== | ||
{{IP sample|IP=IP 71153|count=2}} | {{IP sample|IP=IP 71153|count=2}} | ||
: (1) Unit 2 steam dump and bypass control system malfunction that caused an atmospheric dump valve to open and steam to enter the train A vital 4160 volt switchgear room on November 16, 2018 | : (1) Unit 2 steam dump and bypass control system malfunction that caused an atmospheric dump valve to open and steam to enter the train A vital 4160 volt switchgear room on November 16, 2018 | ||
: (2) Unit 1 automatic reactor trip due to the loss of the train A non-vital 4160 volt bus A1 on December 18, 2018 Licensee Event Reports (3 Samples)=== | : (2) Unit 1 automatic reactor trip due to the loss of the train A non-vital 4160 volt bus A1 on December 18, 2018 | ||
===Licensee Event Reports (3 Samples)=== | |||
The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx: | The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx: | ||
: (1) Licensee Event Report 0500313/2016-003-01, Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1, on December 10, 2018 | : (1) Licensee Event Report 0500313/2016-003-01, Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1, on December 10, 2018 | ||
: (2) Licensee Event Report 0500368/2017-001-00, Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions, on December 10, 2018 | : (2) Licensee Event Report 0500368/2017-001-00, Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions, on December 10, 2018 | ||
: (3) Licensee Event Report 05000313/2018-002-01, Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld, on November 16, | : (3) Licensee Event Report 05000313/2018-002-01, Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld, on November 16, | ||
==INSPECTION RESULTS== | ==INSPECTION RESULTS== | ||
Failure to Fully Implement Vendor Manual Recommended Preventative Maintenance Cornerstone | Failure to Fully Implement Vendor Manual Recommended Preventative Maintenance Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000368/2018004-01 Closed None | ||
==71152 - | ==71152 - Problem== | ||
Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment. | |||
Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing. | Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing. | ||
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Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy, because it was very low safety significance (Green)and was entered into the licensees corrective action program as Condition Reports CR-ANO-2-2018-03442, CR-ANO-2-2018-03454, and CR-ANO-2-2018-03750. | Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy, because it was very low safety significance (Green)and was entered into the licensees corrective action program as Condition Reports CR-ANO-2-2018-03442, CR-ANO-2-2018-03454, and CR-ANO-2-2018-03750. | ||
==71152 - | Observation | ||
==71152 - Problem== | |||
Identification and Resolution Semiannual Trend Review The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site. | |||
The NRC inspectors identified a possible trend associated with the surveillance testing methodology and acceptance criteria. Examples included: | The NRC inspectors identified a possible trend associated with the surveillance testing methodology and acceptance criteria. Examples included: | ||
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* CR-ANO-1-2018-04304. The inspectors identified that Unit 1 Procedure OP-1104.036, Emergency Diesel Generator Operation, Revision 78, did not establish an acceptance criteria for check valve closure testing of diesel starting isolation check valves FO-54A1, FO-55A1, FO-54B1, and FO-55B1. Specifically, the licensee did not determine the maximum allowed check valve leakage to maintain diesel starting air system operability. The licensees corrective action was to determine the appropriate acceptance criteria to assure the valves are, in fact, closed. The licensee and the inspectors validated that the previous test results did not impact diesel starting air system operability. | * CR-ANO-1-2018-04304. The inspectors identified that Unit 1 Procedure OP-1104.036, Emergency Diesel Generator Operation, Revision 78, did not establish an acceptance criteria for check valve closure testing of diesel starting isolation check valves FO-54A1, FO-55A1, FO-54B1, and FO-55B1. Specifically, the licensee did not determine the maximum allowed check valve leakage to maintain diesel starting air system operability. The licensees corrective action was to determine the appropriate acceptance criteria to assure the valves are, in fact, closed. The licensee and the inspectors validated that the previous test results did not impact diesel starting air system operability. | ||
* CR-ANO-C-2018-04296. The inspectors identified a minor violation of Unit 1 TS 5.4.1.a and Unit 2 TS 6.4.1.a for the licensees failure to maintain Unit 1 and Unit 2 Procedure OP-1305.037, Unit 1 Reactor Building Access and Ventilation Leak Rate Testing, Revision 9, and OP-2305.017, Local Leak Rate Testing, Revision 36, respectively. Specifically, the licensee failed to translate Unit 1 TS 5.5.16 and Unit 2 TS 6.5.16 reactor building air lock operability limits as the acceptance criteria into procedures. The licensees corrective actions where to initiate PIFs to translate the TS operability limits as acceptance criteria into the respective procedure. | * CR-ANO-C-2018-04296. The inspectors identified a minor violation of Unit 1 TS 5.4.1.a and Unit 2 TS 6.4.1.a for the licensees failure to maintain Unit 1 and Unit 2 Procedure OP-1305.037, Unit 1 Reactor Building Access and Ventilation Leak Rate Testing, Revision 9, and OP-2305.017, Local Leak Rate Testing, Revision 36, respectively. Specifically, the licensee failed to translate Unit 1 TS 5.5.16 and Unit 2 TS 6.5.16 reactor building air lock operability limits as the acceptance criteria into procedures. The licensees corrective actions where to initiate PIFs to translate the TS operability limits as acceptance criteria into the respective procedure. | ||
* CR-ANO-2-2018-04357. The inspectors identified that Unit 2 Procedure OP-2106.006, Emergency Feedwater System Operations, Revision 98, testing methodology was not in accordance ASME code requirements and did not contain appropriate acceptance criteria for auxiliary feedwater to loop A/B emergency feedwater check valves 2EFW-28, 29, 30, and 31. Specifically, the acceptance criteria for the check valves was if downstream pressure was less than 10 psig or pressure was decreasing, record leakage as zero. The licensees corrective actions are: | * CR-ANO-2-2018-04357. The inspectors identified that Unit 2 Procedure OP-2106.006, Emergency Feedwater System Operations, Revision 98, testing methodology was not in accordance ASME code requirements and did not contain appropriate acceptance criteria for auxiliary feedwater to loop A/B emergency feedwater check valves 2EFW-28, 29, 30, and 31. Specifically, the acceptance criteria for the check valves was if downstream pressure was less than 10 psig or pressure was decreasing, record leakage as zero. The licensees corrective actions are: | ||
===1. Determine the design basis allowed leakage for valves 2EFW-28, 29, 30, and 31=== | |||
and update the procedure and design basis documents. | |||
===2. Initiate a PIF to update the procedure to incorporate appropriate testing methods.=== | |||
In response to the inspectors observations, the licensee entered this trend into their corrective action program for resolution as Condition Report CR-ANO-C-2019-00033. | In response to the inspectors observations, the licensee entered this trend into their corrective action program for resolution as Condition Report CR-ANO-C-2019-00033. | ||
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==71152 - Problem== | ==71152 - Problem== | ||
Identification and Resolution Semiannual Trend Review | |||
The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site. | |||
The inspectors reviewed the corrective action program documentation associated with the common cause analysis of the ANO Unit 1 Refueling Outage 1R27 performance issues, documented in Condition Report CR-ANO-C-2018-02728. The inspectors identified 12 documented human performance errors that caused events, rework, and delays. The licensee initiated the condition report following these events in an effort to document and discover how to prevent these issues from continuing to occur. The licensee identified five causal factors and developed a corrective action for each: | |||
===1. Insufficient ownership and accountability by licensee and supplemental personnel=== | |||
1. Insufficient ownership and accountability by licensee and supplemental personnel resulted in a tolerance of low standards in sustaining nuclear professional behaviors by individual contributors and leadership. Corrective Action (CA) included: | resulted in a tolerance of low standards in sustaining nuclear professional behaviors by individual contributors and leadership. Corrective Action (CA) included: | ||
* Integrate the Own It Accountability Model in work preparation/execution activities into the licensees work preparation meetings to improve ownership and accountability in the pursuit of excellence for licensee work preparation and execution. | * Integrate the Own It Accountability Model in work preparation/execution activities into the licensees work preparation meetings to improve ownership and accountability in the pursuit of excellence for licensee work preparation and execution. | ||
* Implement a licensee Organization Effectiveness Top Issues List and use the organization effectiveness model, administrative tools, and communications media forums to keep issues visible and track to resolution. | * Implement a licensee Organization Effectiveness Top Issues List and use the organization effectiveness model, administrative tools, and communications media forums to keep issues visible and track to resolution. | ||
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===2. Management and peer coaching did not consistently correct unacceptable behaviors=== | ===2. Management and peer coaching did not consistently correct unacceptable behaviors=== | ||
due to the tendency of some leaders to avoid conflict and difficult conversions. | due to the tendency of some leaders to avoid conflict and difficult conversions. | ||
| Line 276: | Line 321: | ||
===3. Licensee personal became complacent to the requirements for strict adherence to=== | ===3. Licensee personal became complacent to the requirements for strict adherence to=== | ||
procedures and work instructions due to the lack of immediate consequence for noncompliance. Corrective actions included: | procedures and work instructions due to the lack of immediate consequence for noncompliance. Corrective actions included: | ||
* Implement remediation model for procedure/work instruction adherence. The intent of this action was to provide clear management expectations and accountability at all levels of the organization for procedure and work instruction adherence. | * Implement remediation model for procedure/work instruction adherence. The intent of this action was to provide clear management expectations and accountability at all levels of the organization for procedure and work instruction adherence. | ||
* Incorporate Procedure EN-HU-106, Procedure and Work Instructions Use and Adherence, Revision 7, training into maintenance continuing training. | * Incorporate Procedure EN-HU-106, Procedure and Work Instructions Use and Adherence, Revision 7, training into maintenance continuing training. | ||
4. Risk was not always recognized or was inappropriately accepted by individuals without sufficient leadership engagement in real time decision-making. Corrective actions included: | ===4. Risk was not always recognized or was inappropriately accepted by individuals without=== | ||
* 2R26 | sufficient leadership engagement in real time decision-making. Corrective actions included: | ||
* | |||
{{a|2R26}} | |||
==2R26 standards team focus on real-time decision-making (stop when unsure). | |||
== | |||
The intent of this action was to ensure the 2R26 standards team plan included a focus area for field observations related to stop when unsure (real-time decision making) and pre-job briefs (work preparation, roles and responsibilities, and risk mitigation). | The intent of this action was to ensure the 2R26 standards team plan included a focus area for field observations related to stop when unsure (real-time decision making) and pre-job briefs (work preparation, roles and responsibilities, and risk mitigation). | ||
5. Licensee leadership did not consistently manage and control outage work scope which impacted the stations ability to effectively prepare and execute scheduled work activities. Corrective actions included: | * | ||
{{a|2R26}} | |||
==2R26 personnel briefing on unknowingly accepting station risk. The intent of== | |||
this action was to provide communication to 2R26 works to increase the awareness of unknowingly making decisions in the field that may increase station risk. | |||
===5. Licensee leadership did not consistently manage and control outage work scope which=== | |||
impacted the stations ability to effectively prepare and execute scheduled work activities. Corrective actions included: | |||
* Validate effective change management when 2R26 major work was reassigned near the outage. The intent of this action was to provide effective change management for scoping transitions that occur within 60 days of schedule start date for 2R26. | * Validate effective change management when 2R26 major work was reassigned near the outage. The intent of this action was to provide effective change management for scoping transitions that occur within 60 days of schedule start date for 2R26. | ||
* Establish unit specific outage work scope priority lists. The intent of this action was clearly defined outage work scope priorities and to control the combined outage work scope within budgeted resources and margins to allow adequate time for work preparation and execution using the prevention model. | * Establish unit specific outage work scope priority lists. The intent of this action was clearly defined outage work scope priorities and to control the combined outage work scope within budgeted resources and margins to allow adequate time for work preparation and execution using the prevention model. | ||
| Line 303: | Line 359: | ||
71111.04 - Equipment Alignment | 71111.04 - Equipment Alignment | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
1-2012-00362 | 1-2012-00362 | ||
1-2012-00363 | |||
1-2018-04976 | |||
C-2016-01706 | |||
Procedures | Procedures | ||
Number | Number | ||
OP-1104.002 | Title | ||
OP-1106.006 | Revision | ||
OP-1107.001 | OP-1104.002 | ||
OP-2106.006 | Makeup and Purification System Operation | ||
OP-1106.006 | |||
Emergency Feedwater Operations | |||
101 | |||
OP-1107.001 | |||
Electrical System Operations | |||
20 | |||
OP-2106.006 | |||
Emergency Feedwater Operations | |||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
EC-65360 | |||
Title | |||
Revision | |||
EC-65360 | |||
CALC-82-D-2086-01 Mark Up to Account for | |||
Condensate Lost due to Pump Bearing and Correct | Condensate Lost due to Pump Bearing and Correct | ||
Computation Error | Computation Error | ||
Calculations | Calculations | ||
Number | Number | ||
CALC-82-D-2086- Volume of CST T-41B Requiring Tornado Missile | Title | ||
Protection | Revision | ||
CALC-82-D-2086- | |||
Volume of CST T-41B Requiring Tornado Missile | |||
Protection | |||
71111.05 - Fire Protection | 71111.05 - Fire Protection | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
2-2018-04226 | 2-2018-04226 | ||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
1A-372-86-G | |||
1B-317-10-EE | Title | ||
1B-335-38-Y | |||
2A-404-2151-A | 1A-372-86-G | ||
Unit 1 Plant Fire Protection | |||
1B-317-10-EE | |||
Unit 1 Plant Fire Protection | |||
1B-335-38-Y | |||
Unit 1 Plant Fire Protection | |||
2A-404-2151-A | |||
Unit 2 Plant Fire Protection | |||
71111.07 - Heat Sink Performance | 71111.07 - Heat Sink Performance | ||
Work Orders | Work Orders | ||
503112 | 503112 | ||
2675121 | |||
2769910 | |||
2770785 | |||
2770786 | |||
Procedures | Procedures | ||
Number | Number | ||
OP-2305.062 | Title | ||
Revision | |||
OP-2305.062 | |||
Service Water System Flow Testing | |||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
EC-72776 | |||
Water Flow Test | Title | ||
Revision | |||
EC-72776 | |||
Document the Results of the 2R25 As-Left Service | |||
Water Flow Test | |||
Calculations | Calculations | ||
Number | Number | ||
CALC-88-E-0032- | Title | ||
Revision | |||
CALC-88-E-0032- | |||
Unit 2 Containment Service Water Cooling Coils Thermal | |||
Performance | Performance | ||
CALC-91-R-2013- | CALC-91-R-2013- | ||
CALC-99-E-0033- | Service Water Performance Testing Methodology | ||
CALC-99-E-0033- | |||
ANO-2 Containment Cooler Fan Motor Horsepower | |||
during a DBA Under Uprate Conditions | during a DBA Under Uprate Conditions | ||
CALC- | CALC- | ||
991522E201-01 | |||
Determination of Error Associated with Air Flow | |||
Measurements of Reactor Building Containment Coolers | |||
71111.11 - Licensed Operator Requalification Program | 71111.11 - Licensed Operator Requalification Program | ||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
A1SXMLOR1902 | |||
Title | |||
Revision | |||
A1SXMLOR1902 | |||
Unit 1 Licensed Operation Requalification Scenario | |||
71111.12 -Maintenance Effectiveness | 71111.12 -Maintenance Effectiveness | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
C-2018-03631 | C-2018-03631 | ||
Work Orders | Work Orders | ||
00486027 | 00486027 | ||
Procedures | Procedures | ||
Number | Number | ||
EN-DC-207 | Title | ||
Revision | |||
EN-DC-207 | |||
Maintenance Rule Periodic Assessment | |||
Drawings | Drawings | ||
Number | Number | ||
E-2258 | Title | ||
M-2001-L1-196 | E-2258 | ||
Schematic Diagram Reactor Control Element Assembly | |||
M-2001-L1-196 | |||
CEDMCS Schematic Diagram Subgroup Filter Panel | |||
Calculations | Calculations | ||
Number | Number | ||
CALC-ANOC-SE- | Title | ||
Revision | |||
CALC-ANOC-SE- | |||
17-00001 | |||
Maintenance Rule 10 CFR 50.65(a)(3) Periodic | |||
Assessment January 1, 2016, to June 30, 2017 | |||
71111.13 - Maintenance Risk Assessments and Emergent Work Control | 71111.13 - Maintenance Risk Assessments and Emergent Work Control | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
2-2018-02847 | 2-2018-02847 | ||
2-2018-02909 | |||
Procedures | Procedures | ||
Number | Number | ||
2102.010 | Title | ||
Revision | |||
2102.010 | |||
Plant Cooldown | |||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
NUREG 1022 | |||
Title | |||
Revision | |||
NUREG 1022 | |||
Event Report Guidelines 10 CFR 50.72 and 50.73 | |||
71111.15 - Operability Determinations and Functionality Assessments | 71111.15 - Operability Determinations and Functionality Assessments | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
1-2015-02718 | 1-2015-02718 | ||
1-2018-04674 | 1-2018-04619 | ||
2-2018-03304 | 1-2018-04636 | ||
1-2018-04668 | |||
1-2018-04671 | |||
1-2018-04674 | |||
2-2013-01190 | |||
2-2018-02976 | |||
2-2018-03127 | |||
2-2018-03252 | |||
2-2018-03304 | |||
Procedures | Procedures | ||
Number | Number | ||
EN-OP-104 | Title | ||
Revision | |||
EN-OP-104 | |||
Operability Determination Process | |||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
EC-79912 | |||
EC-80182 | Title | ||
EC-79906 | |||
N-705 | Date | ||
Degradation in Moderate Energy Class 2 or 3 Vessels | EC-79912 | ||
Engineering Change | |||
EC-80182 | |||
Engineering Change | |||
EC-79906 | |||
Engineering Change | |||
N-705 | |||
Evaluation Criteria for Temporary Acceptance of | |||
Degradation in Moderate Energy Class 2 or 3 Vessels | |||
and Tanks | and Tanks | ||
October 12, | |||
2006 | |||
Calculations | Calculations | ||
Number | Number | ||
CALC-ANO2-ME- | Title | ||
Revision | |||
at ANO2 | CALC-ANO2-ME- | ||
18-00003 | |||
Evaluation of Safety Injection Nozzles and Thermal | |||
Sleeves Supporting Justification for Continued Operation | |||
at ANO2 | |||
Calculations | Calculations | ||
Number | Number | ||
CALC-ANO2-ME- | Title | ||
Revision | |||
at Arkansas Nuclear One Unit 2 | CALC-ANO2-ME- | ||
18-00004 | |||
Operability Assessment for Primary Side Loose Parts | |||
from Migration of Safety Injection Nozzle Thermal Sleeve | |||
at Arkansas Nuclear One Unit 2 | |||
71111.18 - Plant Modifications | 71111.18 - Plant Modifications | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
2-2018-04166 | 2-2018-04166 | ||
Work Orders | Work Orders | ||
471461 | 471461 | ||
2940 | |||
2790774 | |||
Procedures | Procedures | ||
Number | Number | ||
OP-2302.046 | Title | ||
ULD-2-SYS-36 | Revision | ||
OP-2302.046 | |||
CEA Drop Time Test | |||
ULD-2-SYS-36 | |||
Control Element Drive Mechanism | |||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
EC-75702 | |||
Title | |||
Revision | |||
EC-75702 | |||
Replace CEA Upper Gripper Coils with Westinghouse | |||
High Temp Coils | High Temp Coils | ||
EC-78985 | EC-78985 | ||
EC-80516 | Amend Low Voltage Setting for HT Upper Gripper Coils | ||
EC-80516 | |||
ANO-2 CEA Drop Time Uncertainty Relaxation | |||
71111.19 - Post Maintenance Testing | 71111.19 - Post Maintenance Testing | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
1-2018-05315 | 1-2018-05315 | ||
2-2018-04002 | 1-2018-05328 | ||
1-2018-05350 | |||
2-2018-02213 | |||
2-2018-03919 | |||
2-2018-04002 | |||
2-2018-04166 | |||
2-2018-04446 | |||
Work Orders | Work Orders | ||
2399 | 2399 | ||
2790774 | 486741 | ||
509778 | |||
2499 | |||
2940 | |||
2573102 | |||
2776588 | |||
2790774 | |||
2805699 | |||
Procedures | Procedures | ||
Number | Number | ||
OP-2102.001 | Title | ||
OP-2302.046 | Revision | ||
OP-2305.001 | OP-2102.001 | ||
OP-2305.017 | Plant Pre-heatup and Pre-critical Checklist | ||
OP-2302.046 | |||
CEA Drop Time Test | |||
OP-2305.001 | |||
Integrated Engineering Safeguards Test | |||
OP-2305.017 | |||
Local Leak Rate Testing | |||
71111.20 - Refueling and Other Outage Activities | 71111.20 - Refueling and Other Outage Activities | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
1-2018-05325 | 1-2018-05325 | ||
2-2018-02129 | |||
2-2018-02130 | |||
C-2018-04030 | |||
Work Orders | Work Orders | ||
2770782 | 2770782 | ||
Procedure | Procedure | ||
Number | Number | ||
OP-2306.024 | Title | ||
OP-2505.004 | Revision | ||
OP-2306.024 | |||
Unit 2 (IST) Relief Valve Setpoint Testing | |||
OP-2505.004 | |||
Unit 2 Core Support Barrel Removal | |||
71111.22 - Surveillance Testing | 71111.22 - Surveillance Testing | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
1-2018-00963 | 1-2018-00963 | ||
2-2018-04357 | 1-2018-04790 | ||
1-2018-04795 | |||
1-2018-04975 | |||
2-2004-01688 | |||
2-2018-04357 | |||
C-2018-04296 | |||
C-2018-04339 | |||
Work Orders | Work Orders | ||
486741 | 486741 | ||
2815431 | 2573102 | ||
2719205 | |||
2764513 | |||
2770817 | |||
2771820 | |||
2780270 | |||
2815431 | |||
Procedures | Procedures | ||
Number | Number | ||
ER-ANO-2006- | Title | ||
Revision | |||
ER-ANO-2006- | |||
0389-000 | 0389-000 | ||
OP-1305.037 | U2 EFW Alignment to QCST Evaluation | ||
OP-1305.037 | |||
OP-2106.006 | Unit 1 Reactor Building Access and Ventilation Leak | ||
OP-2305.001 | Rate Testing | ||
OP-2305.017 | (8) | ||
SEP-ANO-2-IST-1 Inservice Testing Bases Document | OP-2106.006 | ||
SEP-APJ-002 | Emergency Feedwater System Operation | ||
OP-2305.001 | |||
Integrated Engineering Safeguards Test | |||
OP-2305.017 | |||
Local Leak Rate Testing | |||
SEP-ANO-2-IST-1 Inservice Testing Bases Document | |||
SEP-APJ-002 | |||
Arkansas Nuclear One Containment Leakage Rate | |||
Testing (Appendix J) | Testing (Appendix J) | ||
ULD-2-SYS-12 | ULD-2-SYS-12 | ||
Emergency Feedwater System | |||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
M-2204, Sheet | |||
Title | |||
Revision | |||
M-2204, Sheet | |||
P&ID | P&ID | ||
Emergency Feedwater | |||
Calculations | Calculations | ||
Number | Number | ||
CALC-00-E-0010- | Title | ||
Revision | |||
CALC-00-E-0010- | |||
Appendix J Containment Maximum Allowable Leakage | |||
Rate (La) | Rate (La) | ||
CALC-00-E-0023- | CALC-00-E-0023- | ||
Unit 1 Appendix J Containment Maximum Allowable | |||
Leakage Rate (La) | Leakage Rate (La) | ||
CALC-89-D-2043- | CALC-89-D-2043- | ||
Auxiliary Feedwater Pump | Failure Modes Effect Analysis for the Addition of the | ||
Auxiliary Feedwater Pump | |||
71114.04 - Emergency Action Level and Emergency Plan Changes | 71114.04 - Emergency Action Level and Emergency Plan Changes | ||
Procedures | Procedures | ||
Number | Number | ||
1903.010 | Title | ||
Revision | |||
1903.010 | |||
Emergency Action Level Classification | |||
44, 56 | |||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
0CAN101801 | |||
Title | |||
Date | |||
0CAN101801 | |||
Emergency Plan Implementing Procedure, Arkansas | |||
Nuclear One, Units 1 and 2, | Nuclear One, Units 1 and 2, | ||
Docket Nos. 50-313, 50-368, and 72-13; License | Docket Nos. 50-313, 50-368, and 72-13; License | ||
Nos. DPR-51 and NPF-6 | Nos. DPR-51 and NPF-6 | ||
October 4, 2018 | |||
71151 - Performance Indicator Verification | 71151 - Performance Indicator Verification | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
1-2017-03024 | 1-2017-03024 | ||
1-2018-03729 | |||
Procedures | Procedures | ||
Number | Number | ||
EN-LI-114 | Title | ||
Revision | |||
EN-LI-114 | |||
Regulatory Performance Indicator Process | |||
Calculations | Calculations | ||
Number | Number | ||
CALC-ANO1-SA- | Title | ||
Revision | |||
CALC-ANO1-SA- | |||
16-00001 | 16-00001 | ||
ANO-1 Mitigating System Performance Index Basis | |||
CALC-ANO2-SA- | |||
06-00001 | 06-00001 | ||
ANO-2 Mitigating System Performance Index Basis | |||
71152 - Problem Identification and Resolution | 71152 - Problem Identification and Resolution | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
1-2018-00963 | 1-2018-00963 | ||
2-2018-03442 | 1-2018-04296 | ||
1-2018-03223 | 1-2018-04790 | ||
C-2019-00033 | 1-2018-04975 | ||
C-2018-04339 | |||
2-2018-03442 | |||
2-2018-03442 | |||
2-2018-03454 | |||
2-2018-03750 | |||
2-2009-02997 | |||
1-2018-03223 | |||
2-2018-01009 | |||
1-2018-04304 | |||
C-2018-04296 | |||
2-2018-04357 | |||
C-2019-00033 | |||
Work Orders | Work Orders | ||
411600 | 411600 | ||
511409 | |||
2775094 | |||
Procedures | Procedures | ||
Number | Number | ||
OP-1305.037 | Title | ||
Revision | |||
OP-2416.007 | OP-1305.037 | ||
Unit 1 Reactor Building Access and Ventilation Leak | |||
Rate Testing | |||
(8) | |||
OP-2416.007 | |||
Unit 2 - 2A3 Bus Switchgear Inspection | |||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
PIF 1-18-0125 | |||
Title | |||
PIF 1-18-0125 | |||
Procedure Improvement Form for OP-1305.037 | |||
71153 - Follow-up of Events and Notices of Enforcement Discretion | 71153 - Follow-up of Events and Notices of Enforcement Discretion | ||
Condition Reports (CR-ANO-) | Condition Reports (CR-ANO-) | ||
1-2017-00241 | 1-2017-00241 | ||
1-2018-05340 | 1-2018-05311 | ||
2-2018-04227 | 1-2018-05312 | ||
C-2018-04699 | 1-2018-05326 | ||
1-2018-05332 | |||
1-2018-05340 | |||
1-2018-05360 | |||
2-2017-01555 | |||
2-2018-04225 | |||
2-2018-04226 | |||
2-2018-04227 | |||
2-2018-04230 | |||
2-2018-04241 | |||
2-2018-04244 | |||
2-2018-04336 | |||
C-2018-04699 | |||
Procedures | Procedures | ||
Number | Number | ||
203.012B | Title | ||
EN-OP-126 | Revision | ||
203.012B | |||
Annunciator 2K02 Corrective Action | |||
EN-OP-126 | |||
Post Transient Response and Review | |||
Drawings | Drawings | ||
Number | Number | ||
2HBD-300-1 | Title | ||
2HBD-300-2 | Revision | ||
A-2103 | 2HBD-300-1 | ||
A-2104 | Small Pipe Isometric Auxiliary Building | ||
A-2114 | 2HBD-300-2 | ||
E-34 | Small Pipe Isometric Turbine Building | ||
A-2103 | |||
Architectural Floor Plan at el 368, 372, and 374 6 | |||
A-2104 | |||
Architectural Floor Plan at el 386 | |||
A-2114 | |||
Architectural Exterior Elevations and Sections | |||
E-34 | |||
Schematic Meter and Relay Diagram 4160V System, | |||
Main Supply | Main Supply | ||
M-2112 | M-2112 | ||
M-2116 | Plumbing and Drainage Aux Bldg | ||
M-2116 | |||
Plumbing and Drainage Aux Bldg | |||
Miscellaneous | Miscellaneous | ||
Documents | Documents | ||
Number | Number | ||
STM 2-15 | |||
STM 2-23 | Title | ||
Revision | |||
STM 2-15 | |||
Steam Generators and Main Steam System | |||
STM 2-23 | |||
Steam Dump and Bypass Control System | |||
ML19024A075 | ML19024A075 | ||
SUNSI Review | SUNSI Review | ||
By: NOKeefe | ADAMS: | ||
OFFICE | Non-Publicly Available | ||
NAME | Non-Sensitive | ||
SIGNATURE | Keyword: | ||
DATE | By: NOKeefe | ||
OFFICE | Yes No | ||
NAME | Publicly Available | ||
SIGNATURE | Sensitive | ||
DATE | NRC-002 | ||
OFFICE | |||
SRI:DRP/D | |||
RI:DRP/D | |||
RI:DRP/D | |||
BC:DRS/EB1 | |||
ABC:DRS/EB2 | |||
BC:DRS/OB | |||
NAME | |||
CHenderson | |||
MTobin | |||
TSullivan | |||
VGaddy | |||
JDrake | |||
GWerner | |||
SIGNATURE | |||
cmh | |||
MCT | |||
TMS | |||
vgg | |||
JFD | |||
GEW | |||
DATE | |||
1/10/2019 | |||
1/10/2019 | |||
1/10/2019 | |||
1/14/19 | |||
1/14/19 | |||
01/12/2019 | |||
OFFICE | |||
BC:DRS/PSB2 | |||
ATL:DRS/IPAT | |||
BC:DRP/D | |||
NAME | |||
HGepford | |||
RKellar | |||
NOKeefe | |||
SIGNATURE | |||
hjg | |||
RLK | |||
NFO | |||
DATE | |||
01/14/2019 | |||
01/14/2019 | |||
1/23/19 | |||
}} | }} | ||
Latest revision as of 05:56, 5 January 2025
| ML19024A075 | |
| Person / Time | |
|---|---|
| Site: | Arkansas Nuclear |
| Issue date: | 01/23/2019 |
| From: | O'Keefe N NRC/RGN-IV/DRP/RPB-D |
| To: | Richard Anderson Entergy Operations |
| References | |
| IR 2018004 | |
| Download: ML19024A075 (24) | |
Text
January 23, 2019
SUBJECT:
ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT 05000313/2018004 AND 05000368/2018004
Dear Mr. Anderson:
On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Arkansas Nuclear One, Units 1 and 2. On January 3, 2019, the NRC inspectors discussed the results of this inspection with Mr. J. Kirkpatrick, General Manager of Plant Operations, and other members of your staff. The results of this inspection are documented in the enclosed report.
NRC inspectors documented one finding of very low safety significance (Green) in this report.
This finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.
If you contest the violation or significance of this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the Arkansas Nuclear One. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.
Sincerely,
/RA/
Neil OKeefe, Chief Project Branch D Division of Reactor Projects
Docket Nos. 50-313 and 50-368 License Nos. DPR-51 and NPF-6
Enclosure:
Inspection Report 05000313/2018004 and 05000368/2018004 w/Attachment:
Documents Reviewed
Enclosure U.S. NUCLEAR REGULATORY COMMISSION
Inspection Report
Docket Number(s):
05000313, 05000368
License Number(s):
Report Number(s):
05000313/2018004, 05000368/2018004
Enterprise Identifier: I-2018-004-0005
Licensee:
Entergy Operations, Inc.
Facility:
Arkansas Nuclear One, Units 1 and 2
Location:
Russellville, Arkansas
Inspection Dates:
October 1, 2018 to December 31, 2018
Inspectors:
C. Henderson, Senior Resident Inspector
M. Tobin, Resident Inspector
T. Sullivan, Resident Inspector
R. Bywater, Project Engineer
J. Dixon, Senior Project Engineer
S. Hedger, Emergency Preparedness Inspector
Approved By:
Neil OKeefe
Branch Chief
Division of Reactor Projects
SUMMARY
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Arkansas Nuclear One, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A self-revealed violation and additional items are summarized in the tables below.
List of Findings and Violations
Failure to Fully Implement Vendor Manual Recommended Preventive Maintenance Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000368/2018004-01 Closed None 71152 -
Problem Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment.
Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches because only some electrical contacts were being cleaned. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing.
Additional Tracking Items
Type Issue number Title Inspection Procedure Status LER 0500313/2016-003-01
Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1 71153 Closed LER 0500368/2017-001-00 Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions 71153 Closed LER 05000313/2018-002-01 Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld 71153 Closed
PLANT STATUS
Unit 1 began the inspection period at full power. On November 29, 2018, power was lowered to 85 percent to perform main turbine valve testing and was returned to full power.
On December 18, 2018, Unit 1 had an automatic reactor trip from 100 percent power after the loss of power to non-vital 4160 volt bus A1. On December 21, 2018, Unit 1 commenced a reactor startup and the reactor was made critical. The unit was returned to rated thermal power on December 23, 2018.
Unit 2 began the inspection period in shutdown for Refueling Outage 2R26, which started on September 29, 2018. On November 19, 2018, Unit 2 commenced a reactor startup and the reactor was made critical. The unit was returned to full power on November 24,
INSPECTION SCOPES
Inspections were conducted using the appropriate portions of the inspection procedures (IPs)in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.
Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.
REACTOR SAFETY
71111.04Equipment Alignment Partial Walkdown
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
- (1) Unit 2 train A spent fuel pool cooling during full core offload on November 6, 2018
- (2) Unit 2 train A shutdown cooling system on November 10, 2018
- (3) Unit 1 train A high pressure injection system on November 21, 2018
- (4) Unit 1 and Unit 2 quality condensate storage tank on November 28, 2018
- (5) Unit 2 train A plant protective system on December 31, 2018
71111.05AQFire Protection Annual/Quarterly Quarterly Inspection
The inspectors evaluated fire protection program implementation in the following selected areas:
- (1) Unit 1 emergency feedwater pump area, Fire Area C, Zone 38-Y, on October 23, 2018
- (2) Unit 2 fuel handling area, Fire Area B, Zone 2151-A, on October 23, 2018
- (3) Unit 2 train A 2A3 switchgear room, Fire Area II, Zone 2101-AA, on November 22, 2018
- (4) Unit 2 train A 2B53 switchgear room, Fire Area B, Zone 2091-BB, on November 22, 2018
- (5) Unit 1 north emergency diesel generator room, Fire Area D, Zone 86-G, on November 27, 2018
- (6) Unit 1 east (B) decay heat removal pump room, Fire Area A, Zone 10-EE, on November 28, 2018
71111.07Heat Sink Performance Heat Sink
The inspectors evaluated Unit 2 reactor building containment coolers 2VCC-2A/B/C/D performance on December 17, 2018.
71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification
The inspectors observed and evaluated Unit 1 licensed operator requalification scenario on November 27, 2018.
Operator Performance (2 Samples)
The inspectors observed and evaluated:
- (1) Unit 2 reactor plant startup from Refueling Outage 2R26 on November 19, 2018
- (2) Unit 1 turbine stop valve testing on November 29, 2018
71111.12Maintenance Effectiveness Routine Maintenance Effectiveness
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety-significant functions:
- (1) Unit 1 and Unit 2 50.65(a)(3) periodic evaluation on December 10, 2018
Quality Control (1 Sample)
The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues:
- (1) Unit 2 control element assembly CEA-5 capacitor replacement on December 10, 2018
71111.13Maintenance Risk Assessments and Emergent Work Control
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
- (1) Unit 1 Technical Specification 3.0.3 entry for control room emergency air cleanup system when securing Unit 2 emergency diesel generator 2 on October 31, 2018
- (2) Unit 2 plant protective system maintenance activities on October 31, 2018
- (3) Unit 1 and Unit 2 stator heavy lift from onsite storage area to the barge on November 13, 2018
- (4) Unit 1 emergent work for the loss of the train A non-vital 4160 volt bus A1 troubleshooting and repair on December 18, 2018
71111.15Operability Determinations and Functionality Assessments
The inspectors evaluated the following operability determinations and functionality assessments:
- (1) Unit 2 reactor coolant system thermal sleeves operability assessment on November 2, 2018
- (2) Unit 2 reactor vessel monitoring level system detector (RadCal) operability assessment on November 26, 2018
- (3) Unit 1 sodium hydroxide spray additive system tank pitting below minimum wall thickness operability assessment on December 12, 2018
71111.18Plant Modifications
The inspectors evaluated the following permanent modifications:
- (1) Unit 2 control element assembly upper gripper coil stack replacements on October 26, 2018
- (2) Unit 2 removal of timing uncertainty from the control element assembly drop time test on December 31, 2018
71111.19Post Maintenance Testing
The inspectors evaluated the following post-maintenance tests:
- (1) Unit 2 rod drop timing surveillance November 16, 2018
- (2) Unit 2 valve 2CV-5255-1 as left local leak-rate test on November 17, 2018
- (3) Unit 2 control element assembly CEA-5 capacitor replacement and control element assembly upper gripper coil replacement on November 17, 2018
- (4) Unit 2 reactor vessel monitoring level system detector (Radcal) replacement on November 20, 2018
- (5) Unit 2 check valve 2SI-14A inspection due to valve chattering on November 27, 2018
- (6) Unit 1 main feedwater block isolation valves repair on December 18, 2018
- (7) Unit 2 restoration of lifted electrical leads during integrated safeguards testing on December 31, 2018
71111.20Refueling and Other Outage Activities
- (1) The inspectors evaluated Unit 2 Refueling Outage 2R26 activities from September 29 to November 2, 2018.
- (2) The inspectors evaluated Unit 1 Forced Outage 2018-002 activities from December 18 to December 21, 2018.
===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests:
Routine===
- (1) Unit 2 reactor vessel foreign object search and retrieval on October 23, 2018
- (2) Unit 1 and Unit 2 personnel airlock door seal leakage testing on October 23, 2018
- (3) Unit 2 rod drop testing on November 14, 2018
- (4) Unit 2 as-found local leak-rate test for valve 2CV-5255-1 on November 16, 2018
- (5) Unit 2 integrated safety system testing on November 16, 2018
- (6) Unit 2 emergency feedwater check valves 2EFW-28, 29, 30, and 31, on December 14, 2018
71114.04Emergency Action Level and Emergency Plan Changes
The licensee submitted a summary of Emergency Action Level classification procedure changes (Revision 57) to the NRC on October 4, 2018. The inspector conducted an in-office review of the changes from December 4, 2018, to December 14, 2018. This evaluation does not constitute NRC approval.
OTHER ACTIVITIES - BASELINE
71151Performance Indicator Verification
The inspectors verified licensee performance indicators submittals listed below:
- (1) MS09: Unit 1 and Unit 2 Residual Heat Removal Systems (10/01/2017-09/30/2018)
- (2) MS10: Unit 1 and Unit 2 Cooling Water Support Systems (10/01/2017-09/30/2018)
71152Problem Identification and Resolution Semiannual Trend Review
The inspectors reviewed the licensees corrective action program for trends that might be indicative of more significant safety issues:
- (1) Procedural quality involving the adequacy of surveillance testing acceptance criteria and testing methodology
- (2) Common cause analysis of the ANO Unit 1 Refueling Outage 1R27 human performance issues, Condition Report CR-ANO-C-2018-02728
Annual Follow-up of Selected Issues (1 Sample)
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
- (1) Unit 2 failure of train A safety-related 4160 volt breaker 2A-303 to automatically close and service water pump B to start during surveillance testing on December 17, 2018
71153Follow-up of Events and Notices of Enforcement Discretion Events
- (1) Unit 2 steam dump and bypass control system malfunction that caused an atmospheric dump valve to open and steam to enter the train A vital 4160 volt switchgear room on November 16, 2018
- (2) Unit 1 automatic reactor trip due to the loss of the train A non-vital 4160 volt bus A1 on December 18, 2018
Licensee Event Reports (3 Samples)
The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
- (1) Licensee Event Report 0500313/2016-003-01, Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1, on December 10, 2018
- (2) Licensee Event Report 0500368/2017-001-00, Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions, on December 10, 2018
- (3) Licensee Event Report 05000313/2018-002-01, Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld, on November 16,
INSPECTION RESULTS
Failure to Fully Implement Vendor Manual Recommended Preventative Maintenance Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000368/2018004-01 Closed None
71152 - Problem
Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment.
Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing.
Description:
On October 23, 2018, the train A safety-related 4160 V switchgear 2A-303 breaker that provides power to pump 2P-4B failed to automatically close and start pump 2P-4B during surveillance testing. It was determined that an interlock on the train A safety-related 4160 V switchgear 2A-302 breaker that powers train A service water pump (2P-4A) prevented 2A-303 from automatically closing and starting pump 2P-4B. This interlock is designed to prevent both the 2P-4A and 2P-4B pumps from both automatically starting when aligned to emergency diesel generator 1. The interlock was comprised of a shunt trip attachment (STA) switch in the 2A-302 breaker. The licensee entered this issue into their corrective action program as Condition Report CR-ANO-2-2018-03454.
The licensee performed an equipment failure evaluation, documented in Condition Report CR-ANO-2-2018-03454, and determined that an oxide layer on the contacts of the STA switch for the 2A-302 breaker was the cause of the failure of 2A-303 to automatically close and start pump 2P-4B. A review of STA switch failures in the previous 10 years revealed that in 2009, a similar failure occurred and the corrective action was to incorporate vendor manual instructions to inspect and, if necessary, burnish (clean) the contacts when performing Procedure OP-2416.007, Unit 2 - 2A3 Bus Switchgear Inspection, Revision 17.
The licensee added this step into the work instructions to minimize oxide layer formation that would prevent the contacts on the STA switch from functioning. However, the updated work instructions did not fully incorporate the vendor manual recommended preventive maintenance. Specifically, the work instructions only gave instructions on how to clean the outer set of contacts and did not include direction on how to clean the harder to reach inner contacts. The licensee determined that the inner contacts were dirty and had caused the interlock to fail in this case.
The inspectors determined that this failure did not result in a technical specification violation because 2P-4B is a swing pump that could be powered from and connected to either train; during the period when it was assumed that it could not be started from the train A bus, the train A pump 2P-4A was in service and credited for technical specification compliance.
Corrective Actions: The licensee moved the interlock from the failed contact to a spare contact that they verified to be in good condition to restore operability of the pump. The licensee also performed an extent of condition evaluation to identify other failed safety-related and important to safety breakers. While several other contacts were in a condition that warranted cleaning, all of the other breakers tested would have functioned correctly if needed.
Corrective Action References: The licensee entered this issue into their corrective action program as Condition Reports CR-ANO-2-2018-03442, CR-ANO-2-2018-03454, and CR-ANO-2-2018-03750.
Performance Assessment:
Performance Deficiency: The licensees failure to fully implement vendor manual recommended preventive maintenance for STA contact switches is a performance deficiency.
Specifically, the licensee failed to provide maintenance instructions to clean the inner STA switch contacts that were in use, allowing them to become oxidized and develop a high resistance.
Screening: The inspectors determined the performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the swing safety-related 4160 volt breaker 2A-303 was nonfunctional due to not fully implementing vendor recommended preventive maintenance on the inner half of the STA switches.
Significance: Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 2, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because the finding:
- (1) was not a design or qualification deficiency;
- (2) did not represent a loss of system and/or function;
- (3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and
- (4) did not result in the loss of a high safety-significant, nontechnical specification train. Specifically, the 2P-4B pump was never credited for technical specification compliance during the period when it would not automatically start from the train A bus.
Cross-cutting Aspect: A cross-cutting aspect was not assigned to this finding because the performance deficiency occurred in 2009, and therefore was not indicative of current plant performance.
Enforcement:
Violation: Technical Specification 6.4.1.a for Unit 2 requires, in part, that written procedures be established, implemented, and maintained covering the applicable procedures listed in Appendix A to Regulatory Guide 1.33, Quality Assurance Program Requirements, Revision 2, dated February 1978. Regulatory Guide 1.33, Appendix A, Section 9.a, states, in part, that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.
Contrary to the above, between October 2009 and October 2018, the licensee failed to properly pre-plan and perform maintenance that can affect performance of safety-related equipment in accordance with written procedures, document instructions, or drawings appropriate to the circumstances. Specifically, the licensee failed to maintain adequate work instructions to fully implement vendor recommended maintenance for safety-related breaker STA switch contacts when performing Procedure OP-2416.007, Unit 2 - 2A3 Bus Switchgear Inspection, Revision 17, Supplement 1, 2A3 Bus and Cubicle Inspection and Cleaning.
This condition led to the failure of the swing service water pump 2P-4B to automatically start during surveillance testing on October 23, 2018.
Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy, because it was very low safety significance (Green)and was entered into the licensees corrective action program as Condition Reports CR-ANO-2-2018-03442, CR-ANO-2-2018-03454, and CR-ANO-2-2018-03750.
Observation
71152 - Problem
Identification and Resolution Semiannual Trend Review The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site.
The NRC inspectors identified a possible trend associated with the surveillance testing methodology and acceptance criteria. Examples included:
- CR-ANO-1-2018-03223 and CR-ANO-2-2018-01009. The inspectors identified a minor violation of Unit 1 Technical Specification (TS) 5.4.1.a and Unit 2 TS 6.4.1.a for the licensees failure to maintain Unit 1 and Unit 2 Procedure OP-1102.001, Plant Pre-heat up and Pre-critical Checklist, Revision 83, and OP-2102.001, Plant Pre-heat up and Pre-critical Checklist, Revision 87, respectively. Specifically, the licensee did not actually measure seat leakage for some of the reactor coolant system (RCS)primary isolation valves (PIV) included in this surveillance test in accordance with American Society of Mechanical Engineers (ASME) Subsection ISTC-3630(c), Seat Leakage Measurement. The inspectors identified that the procedure inappropriately allowed recording a value of zero for the leak rate of several valves based on the measurements taken from the upstream check valve. The licensees corrective actions where to initiate procedure improvement forms to establish procedural steps to actually measure seat leakage in accordance with ASME Subsection ISTC-3630(c).
- CR-ANO-1-2018-04304. The inspectors identified that Unit 1 Procedure OP-1104.036, Emergency Diesel Generator Operation, Revision 78, did not establish an acceptance criteria for check valve closure testing of diesel starting isolation check valves FO-54A1, FO-55A1, FO-54B1, and FO-55B1. Specifically, the licensee did not determine the maximum allowed check valve leakage to maintain diesel starting air system operability. The licensees corrective action was to determine the appropriate acceptance criteria to assure the valves are, in fact, closed. The licensee and the inspectors validated that the previous test results did not impact diesel starting air system operability.
- CR-ANO-C-2018-04296. The inspectors identified a minor violation of Unit 1 TS 5.4.1.a and Unit 2 TS 6.4.1.a for the licensees failure to maintain Unit 1 and Unit 2 Procedure OP-1305.037, Unit 1 Reactor Building Access and Ventilation Leak Rate Testing, Revision 9, and OP-2305.017, Local Leak Rate Testing, Revision 36, respectively. Specifically, the licensee failed to translate Unit 1 TS 5.5.16 and Unit 2 TS 6.5.16 reactor building air lock operability limits as the acceptance criteria into procedures. The licensees corrective actions where to initiate PIFs to translate the TS operability limits as acceptance criteria into the respective procedure.
- CR-ANO-2-2018-04357. The inspectors identified that Unit 2 Procedure OP-2106.006, Emergency Feedwater System Operations, Revision 98, testing methodology was not in accordance ASME code requirements and did not contain appropriate acceptance criteria for auxiliary feedwater to loop A/B emergency feedwater check valves 2EFW-28, 29, 30, and 31. Specifically, the acceptance criteria for the check valves was if downstream pressure was less than 10 psig or pressure was decreasing, record leakage as zero. The licensees corrective actions are:
1. Determine the design basis allowed leakage for valves 2EFW-28, 29, 30, and 31
and update the procedure and design basis documents.
2. Initiate a PIF to update the procedure to incorporate appropriate testing methods.
In response to the inspectors observations, the licensee entered this trend into their corrective action program for resolution as Condition Report CR-ANO-C-2019-00033.
Observation
71152 - Problem
Identification and Resolution Semiannual Trend Review
The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site.
The inspectors reviewed the corrective action program documentation associated with the common cause analysis of the ANO Unit 1 Refueling Outage 1R27 performance issues, documented in Condition Report CR-ANO-C-2018-02728. The inspectors identified 12 documented human performance errors that caused events, rework, and delays. The licensee initiated the condition report following these events in an effort to document and discover how to prevent these issues from continuing to occur. The licensee identified five causal factors and developed a corrective action for each:
1. Insufficient ownership and accountability by licensee and supplemental personnel
resulted in a tolerance of low standards in sustaining nuclear professional behaviors by individual contributors and leadership. Corrective Action (CA) included:
- Integrate the Own It Accountability Model in work preparation/execution activities into the licensees work preparation meetings to improve ownership and accountability in the pursuit of excellence for licensee work preparation and execution.
- Implement a licensee Organization Effectiveness Top Issues List and use the organization effectiveness model, administrative tools, and communications media forums to keep issues visible and track to resolution.
- Pursuit of Craftsmanship Excellence Committee. The pursuit of craftsmanship excellence through the engagement and ownership of supplemental personnel focused on improving craftsmanship, work quality, maintenance technical fundamentals, and sustaining nuclear professional behaviors.
- Senior leadership team to partner with the first line supervisors leadership council to promote greater ownership, engagement and accountability to address licensee top first-line supervisory issues.
- Conduct a Unit 2 Refueling Outage 2R26 pre-outage leadership and alignment meeting with licensee and supplemental leaders to reset the standards and expectations for 2R26 work preparation and execution.
2. Management and peer coaching did not consistently correct unacceptable behaviors
due to the tendency of some leaders to avoid conflict and difficult conversions.
Corrective actions included:
- Manager leadership by example and field presence. The intent of this action was to drive and set an example for management oversight of the preparation and execution of outage maintenance critical activities.
- Reinforce the expectations for detailed pre-job briefs and perform observations focused on pre-job briefs to validate standards are met. The intent of this action was to verify monthly that licensee and supplemental leader observation quality was documented in accordance with the observation excellence model and to provide coaching to correct identified gaps.
- Incorporate observation goals into the 2018 personnel performance reviews.
The intent of this action was to ensure leaders are driving the right behavior changes in the organization.
- Commence rapid trending of observation data.
3. Licensee personal became complacent to the requirements for strict adherence to
procedures and work instructions due to the lack of immediate consequence for noncompliance. Corrective actions included:
- Implement remediation model for procedure/work instruction adherence. The intent of this action was to provide clear management expectations and accountability at all levels of the organization for procedure and work instruction adherence.
- Incorporate Procedure EN-HU-106, Procedure and Work Instructions Use and Adherence, Revision 7, training into maintenance continuing training.
4. Risk was not always recognized or was inappropriately accepted by individuals without
sufficient leadership engagement in real time decision-making. Corrective actions included:
==2R26 standards team focus on real-time decision-making (stop when unsure).
==
The intent of this action was to ensure the 2R26 standards team plan included a focus area for field observations related to stop when unsure (real-time decision making) and pre-job briefs (work preparation, roles and responsibilities, and risk mitigation).
2R26 personnel briefing on unknowingly accepting station risk. The intent of
this action was to provide communication to 2R26 works to increase the awareness of unknowingly making decisions in the field that may increase station risk.
5. Licensee leadership did not consistently manage and control outage work scope which
impacted the stations ability to effectively prepare and execute scheduled work activities. Corrective actions included:
- Validate effective change management when 2R26 major work was reassigned near the outage. The intent of this action was to provide effective change management for scoping transitions that occur within 60 days of schedule start date for 2R26.
- Establish unit specific outage work scope priority lists. The intent of this action was clearly defined outage work scope priorities and to control the combined outage work scope within budgeted resources and margins to allow adequate time for work preparation and execution using the prevention model.
- Perform an independent verification that major projects are ready for execution prior to 2R26. The intent of this action was clearly defined outage work scope priorities and control the combined outage work scope within budgeted resources and margins to allow adequate time for work preparation and execution using the prevention model.
The inspectors observed actions implemented during ANO Unit 2 Refueling Outage 2R26 and noted that the number of events, rework, and delays decreased dramatically during Refueling Outage 2R26 as a result. Although several performance issues still occurred, the inspectors determined that the ongoing actions to minimize these issues are being implemented successfully. For this trend, the inspectors determined that the licensee had identified the trend, completed an appropriate evaluation, and had taken actions to correct the identified trend.
EXIT MEETINGS AND DEBRIEFS
On December 14, 2018, the inspector presented the emergency action level revision review inspection results to Mr. A. Sherrill, Manager, Emergency Preparedness, and other members of the licensee staff. The inspectors verified no proprietary information was retained or documented in this report.
On January 3, 2019, the inspector presented the quarterly resident inspector inspection results to Mr. J. Kirkpatrick, General Manager of Plant Operations, and other members of the licensee staff. The inspectors verified no proprietary information was retained or documented in this report.
DOCUMENTS REVIEWED
71111.04 - Equipment Alignment
Condition Reports (CR-ANO-)
1-2012-00362
1-2012-00363
1-2018-04976
C-2016-01706
Procedures
Number
Title
Revision
OP-1104.002
Makeup and Purification System Operation
OP-1106.006
Emergency Feedwater Operations
101
OP-1107.001
Electrical System Operations
20
OP-2106.006
Emergency Feedwater Operations
Miscellaneous
Documents
Number
Title
Revision
CALC-82-D-2086-01 Mark Up to Account for
Condensate Lost due to Pump Bearing and Correct
Computation Error
Calculations
Number
Title
Revision
CALC-82-D-2086-
Volume of CST T-41B Requiring Tornado Missile
Protection
71111.05 - Fire Protection
Condition Reports (CR-ANO-)
2-2018-04226
Miscellaneous
Documents
Number
Title
Unit 1 Plant Fire Protection
Unit 1 Plant Fire Protection
Unit 1 Plant Fire Protection
Unit 2 Plant Fire Protection
71111.07 - Heat Sink Performance
Work Orders
503112
2675121
2769910
2770785
2770786
Procedures
Number
Title
Revision
OP-2305.062
Service Water System Flow Testing
Miscellaneous
Documents
Number
Title
Revision
Document the Results of the 2R25 As-Left Service
Water Flow Test
Calculations
Number
Title
Revision
CALC-88-E-0032-
Unit 2 Containment Service Water Cooling Coils Thermal
Performance
CALC-91-R-2013-
Service Water Performance Testing Methodology
CALC-99-E-0033-
ANO-2 Containment Cooler Fan Motor Horsepower
during a DBA Under Uprate Conditions
CALC-
991522E201-01
Determination of Error Associated with Air Flow
Measurements of Reactor Building Containment Coolers
71111.11 - Licensed Operator Requalification Program
Miscellaneous
Documents
Number
Title
Revision
A1SXMLOR1902
Unit 1 Licensed Operation Requalification Scenario
71111.12 -Maintenance Effectiveness
Condition Reports (CR-ANO-)
C-2018-03631
Work Orders
00486027
Procedures
Number
Title
Revision
Maintenance Rule Periodic Assessment
Drawings
Number
Title
E-2258
Schematic Diagram Reactor Control Element Assembly
M-2001-L1-196
CEDMCS Schematic Diagram Subgroup Filter Panel
Calculations
Number
Title
Revision
CALC-ANOC-SE-
17-00001
Maintenance Rule 10 CFR 50.65(a)(3) Periodic
Assessment January 1, 2016, to June 30, 2017
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Condition Reports (CR-ANO-)
2-2018-02847
2-2018-02909
Procedures
Number
Title
Revision
2102.010
Plant Cooldown
Miscellaneous
Documents
Number
Title
Revision
Event Report Guidelines 10 CFR 50.72 and 50.73
71111.15 - Operability Determinations and Functionality Assessments
Condition Reports (CR-ANO-)
1-2015-02718
1-2018-04619
1-2018-04636
1-2018-04668
1-2018-04671
1-2018-04674
2-2013-01190
2-2018-02976
2-2018-03127
2-2018-03252
2-2018-03304
Procedures
Number
Title
Revision
Operability Determination Process
Miscellaneous
Documents
Number
Title
Date
Engineering Change
Engineering Change
Engineering Change
N-705
Evaluation Criteria for Temporary Acceptance of
Degradation in Moderate Energy Class 2 or 3 Vessels
and Tanks
October 12,
2006
Calculations
Number
Title
Revision
CALC-ANO2-ME-
18-00003
Evaluation of Safety Injection Nozzles and Thermal
Sleeves Supporting Justification for Continued Operation
at ANO2
Calculations
Number
Title
Revision
CALC-ANO2-ME-
18-00004
Operability Assessment for Primary Side Loose Parts
from Migration of Safety Injection Nozzle Thermal Sleeve
at Arkansas Nuclear One Unit 2
71111.18 - Plant Modifications
Condition Reports (CR-ANO-)
2-2018-04166
Work Orders
471461
2940
2790774
Procedures
Number
Title
Revision
OP-2302.046
CEA Drop Time Test
ULD-2-SYS-36
Control Element Drive Mechanism
Miscellaneous
Documents
Number
Title
Revision
Replace CEA Upper Gripper Coils with Westinghouse
High Temp Coils
Amend Low Voltage Setting for HT Upper Gripper Coils
ANO-2 CEA Drop Time Uncertainty Relaxation
71111.19 - Post Maintenance Testing
Condition Reports (CR-ANO-)
1-2018-05315
1-2018-05328
1-2018-05350
2-2018-02213
2-2018-03919
2-2018-04002
2-2018-04166
2-2018-04446
Work Orders
2399
486741
509778
2499
2940
2573102
2776588
2790774
2805699
Procedures
Number
Title
Revision
OP-2102.001
Plant Pre-heatup and Pre-critical Checklist
OP-2302.046
CEA Drop Time Test
OP-2305.001
Integrated Engineering Safeguards Test
OP-2305.017
71111.20 - Refueling and Other Outage Activities
Condition Reports (CR-ANO-)
1-2018-05325
2-2018-02129
2-2018-02130
C-2018-04030
Work Orders
2770782
Procedure
Number
Title
Revision
OP-2306.024
Unit 2 (IST) Relief Valve Setpoint Testing
OP-2505.004
Unit 2 Core Support Barrel Removal
71111.22 - Surveillance Testing
Condition Reports (CR-ANO-)
1-2018-00963
1-2018-04790
1-2018-04795
1-2018-04975
2-2004-01688
2-2018-04357
C-2018-04296
C-2018-04339
Work Orders
486741
2573102
2719205
2764513
2770817
2771820
2780270
2815431
Procedures
Number
Title
Revision
ER-ANO-2006-
0389-000
U2 EFW Alignment to QCST Evaluation
OP-1305.037
Unit 1 Reactor Building Access and Ventilation Leak
Rate Testing
(8)
OP-2106.006
Emergency Feedwater System Operation
OP-2305.001
Integrated Engineering Safeguards Test
OP-2305.017
SEP-ANO-2-IST-1 Inservice Testing Bases Document
SEP-APJ-002
Arkansas Nuclear One Containment Leakage Rate
Testing (Appendix J)
ULD-2-SYS-12
Miscellaneous
Documents
Number
Title
Revision
M-2204, Sheet
Emergency Feedwater
Calculations
Number
Title
Revision
CALC-00-E-0010-
Appendix J Containment Maximum Allowable Leakage
Rate (La)
CALC-00-E-0023-
Unit 1 Appendix J Containment Maximum Allowable
Leakage Rate (La)
CALC-89-D-2043-
Failure Modes Effect Analysis for the Addition of the
Auxiliary Feedwater Pump
71114.04 - Emergency Action Level and Emergency Plan Changes
Procedures
Number
Title
Revision
1903.010
Emergency Action Level Classification
44, 56
Miscellaneous
Documents
Number
Title
Date
0CAN101801
Emergency Plan Implementing Procedure, Arkansas
Nuclear One, Units 1 and 2,
Docket Nos. 50-313, 50-368, and 72-13; License
October 4, 2018
71151 - Performance Indicator Verification
Condition Reports (CR-ANO-)
1-2017-03024
1-2018-03729
Procedures
Number
Title
Revision
Regulatory Performance Indicator Process
Calculations
Number
Title
Revision
CALC-ANO1-SA-
16-00001
ANO-1 Mitigating System Performance Index Basis
CALC-ANO2-SA-
06-00001
ANO-2 Mitigating System Performance Index Basis
71152 - Problem Identification and Resolution
Condition Reports (CR-ANO-)
1-2018-00963
1-2018-04296
1-2018-04790
1-2018-04975
C-2018-04339
2-2018-03442
2-2018-03442
2-2018-03454
2-2018-03750
2-2009-02997
1-2018-03223
2-2018-01009
1-2018-04304
C-2018-04296
2-2018-04357
C-2019-00033
Work Orders
411600
511409
2775094
Procedures
Number
Title
Revision
OP-1305.037
Unit 1 Reactor Building Access and Ventilation Leak
Rate Testing
(8)
OP-2416.007
Unit 2 - 2A3 Bus Switchgear Inspection
Miscellaneous
Documents
Number
Title
PIF 1-18-0125
Procedure Improvement Form for OP-1305.037
71153 - Follow-up of Events and Notices of Enforcement Discretion
Condition Reports (CR-ANO-)
1-2017-00241
1-2018-05311
1-2018-05312
1-2018-05326
1-2018-05332
1-2018-05340
1-2018-05360
2-2017-01555
2-2018-04225
2-2018-04226
2-2018-04227
2-2018-04230
2-2018-04241
2-2018-04244
2-2018-04336
C-2018-04699
Procedures
Number
Title
Revision
203.012B
Annunciator 2K02 Corrective Action
Post Transient Response and Review
Drawings
Number
Title
Revision
Small Pipe Isometric Auxiliary Building
Small Pipe Isometric Turbine Building
A-2103
Architectural Floor Plan at el 368, 372, and 374 6
A-2104
Architectural Floor Plan at el 386
A-2114
Architectural Exterior Elevations and Sections
E-34
Schematic Meter and Relay Diagram 4160V System,
Main Supply
M-2112
Plumbing and Drainage Aux Bldg
M-2116
Plumbing and Drainage Aux Bldg
Miscellaneous
Documents
Number
Title
Revision
STM 2-15
Steam Generators and Main Steam System
STM 2-23
Steam Dump and Bypass Control System
SUNSI Review
ADAMS:
Non-Publicly Available
Non-Sensitive
Keyword:
By: NOKeefe
Yes No
Publicly Available
Sensitive
OFFICE
SRI:DRP/D
RI:DRP/D
RI:DRP/D
BC:DRS/EB1
ABC:DRS/EB2
BC:DRS/OB
NAME
CHenderson
MTobin
TSullivan
VGaddy
JDrake
GWerner
SIGNATURE
cmh
MCT
vgg
JFD
GEW
DATE
1/10/2019
1/10/2019
1/10/2019
1/14/19
1/14/19
01/12/2019
OFFICE
BC:DRS/PSB2
ATL:DRS/IPAT
BC:DRP/D
NAME
HGepford
RKellar
NOKeefe
SIGNATURE
hjg
RLK
DATE
01/14/2019
01/14/2019
1/23/19