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=Text=
=Text=
{{#Wiki_filter:ary 23, 2019
{{#Wiki_filter:January 23, 2019


==SUBJECT:==
==SUBJECT:==
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Sincerely,
Sincerely,
/RA/
/RA/  
Neil OKeefe, Chief Project Branch D Division of Reactor Projects Docket Nos. 50-313 and 50-368 License Nos. DPR-51 and NPF-6 Enclosure:
 
Neil OKeefe, Chief Project Branch D Division of Reactor Projects  
 
Docket Nos. 50-313 and 50-368 License Nos. DPR-51 and NPF-6  
 
Enclosure:
Inspection Report 05000313/2018004 and 05000368/2018004 w/Attachment:
Inspection Report 05000313/2018004 and 05000368/2018004 w/Attachment:
Documents Reviewed
Documents Reviewed  


U.S. NUCLEAR REGULATORY COMMISSION
Enclosure U.S. NUCLEAR REGULATORY COMMISSION  


==Inspection Report==
==Inspection Report==
Docket Number(s): 05000313, 05000368 License Number(s): DPR-51, NPF-6 Report Number(s): 05000313/2018004, 05000368/2018004 Enterprise Identifier: I-2018-004-0005 Licensee: Entergy Operations, Inc.
Docket Number(s):
05000313, 05000368  
 
License Number(s):
DPR-51, NPF-6  
 
Report Number(s):
05000313/2018004, 05000368/2018004  
 
Enterprise Identifier: I-2018-004-0005  
 
Licensee:
Entergy Operations, Inc.  
 
Facility:
Arkansas Nuclear One, Units 1 and 2
 
Location:
Russellville, Arkansas
 
Inspection Dates:
October 1, 2018 to December 31, 2018


Facility: Arkansas Nuclear One, Units 1 and 2 Location: Russellville, Arkansas Inspection Dates: October 1, 2018 to December 31, 2018 Inspectors: C. Henderson, Senior Resident Inspector M. Tobin, Resident Inspector T. Sullivan, Resident Inspector R. Bywater, Project Engineer J. Dixon, Senior Project Engineer S. Hedger, Emergency Preparedness Inspector Approved By: Neil OKeefe Branch Chief Division of Reactor Projects Enclosure
Inspectors:
C. Henderson, Senior Resident Inspector
M. Tobin, Resident Inspector
T. Sullivan, Resident Inspector
R. Bywater, Project Engineer
J. Dixon, Senior Project Engineer
S. Hedger, Emergency Preparedness Inspector  
 
Approved By:
Neil OKeefe
Branch Chief
Division of Reactor Projects  


=SUMMARY=
=SUMMARY=
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Arkansas Nuclear One, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A self-revealed violation and additional items are summarized in the tables below.
The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Arkansas Nuclear One, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A self-revealed violation and additional items are summarized in the tables below.


List of Findings and Violations Failure to Fully Implement Vendor Manual Recommended Preventive Maintenance Cornerstone       Significance                                         Cross-     Inspection cutting    Procedure Aspect Mitigating       Green                                               None        71152 -
===List of Findings and Violations===
Systems          NCV 05000368/2018004-01                                         Problem Closed                                                          Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment.
Failure to Fully Implement Vendor Manual Recommended Preventive Maintenance Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000368/2018004-01 Closed None 71152 -
Problem Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment.


Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches because only some electrical contacts were being cleaned. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing.
Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches because only some electrical contacts were being cleaned. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing.


Additional Tracking Items Type     Issue number                 Title                         Inspection     Status Procedure LER       0500313/2016-003-01         Tornado Vulnerabilities       71153          Closed Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1 LER       0500368/2017-001-00         Inadequate Protection from     71153          Closed Tornado Missiles Identified Due to Nonconforming Design Conditions LER       05000313/2018-002-01         Leak in Class 1 Reactor       71153          Closed Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld
===Additional Tracking Items===
Type Issue number Title Inspection Procedure Status LER 0500313/2016-003-01  
 
Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1 71153 Closed LER 0500368/2017-001-00 Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions 71153 Closed LER 05000313/2018-002-01 Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld 71153 Closed


=PLANT STATUS=
=PLANT STATUS=


===Unit 1 began the inspection period at full power. On November 29, 2018, power was lowered to 85 percent to perform main turbine valve testing and was returned to full power.
Unit 1 began the inspection period at full power. On November 29, 2018, power was lowered to 85 percent to perform main turbine valve testing and was returned to full power.


On December 18, 2018, Unit 1 had an automatic reactor trip from 100 percent power after the loss of power to non-vital 4160 volt bus A1. On December 21, 2018, Unit 1 commenced a reactor startup and the reactor was made critical. The unit was returned to rated thermal power on December 23, 2018.
On December 18, 2018, Unit 1 had an automatic reactor trip from 100 percent power after the loss of power to non-vital 4160 volt bus A1. On December 21, 2018, Unit 1 commenced a reactor startup and the reactor was made critical. The unit was returned to rated thermal power on December 23, 2018.


Unit 2 began the inspection period in shutdown for Refueling Outage 2R26, which started on September 29, 2018. On November 19, 2018, Unit 2 commenced a reactor startup and the reactor was made critical. The unit was returned to full power on November 24, 2018.
Unit 2 began the inspection period in shutdown for Refueling Outage 2R26, which started on September 29, 2018. On November 19, 2018, Unit 2 commenced a reactor startup and the reactor was made critical. The unit was returned to full power on November 24,


==INSPECTION SCOPES==
==INSPECTION SCOPES==
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==REACTOR SAFETY==
==REACTOR SAFETY==
 
===71111.04Equipment Alignment Partial Walkdown===
===71111.04Equipment Alignment Partial Walkdown ===
{{IP sample|IP=IP 71111.04|count=5}}
{{IP sample|IP=IP 71111.04|count=5}}
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:
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: (3) Unit 1 train A high pressure injection system on November 21, 2018
: (3) Unit 1 train A high pressure injection system on November 21, 2018
: (4) Unit 1 and Unit 2 quality condensate storage tank on November 28, 2018
: (4) Unit 1 and Unit 2 quality condensate storage tank on November 28, 2018
: (5) Unit 2 train A plant protective system on December 31, 2018
: (5) Unit 2 train A plant protective system on December 31, 2018  


===71111.05AQFire Protection Annual/Quarterly Quarterly Inspection ===
===71111.05AQFire Protection Annual/Quarterly Quarterly Inspection===
{{IP sample|IP=IP 71111.05|count=6}}
{{IP sample|IP=IP 71111.05|count=6}}
The inspectors evaluated fire protection program implementation in the following selected areas:
The inspectors evaluated fire protection program implementation in the following selected areas:
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: (4) Unit 2 train A 2B53 switchgear room, Fire Area B, Zone 2091-BB, on November 22, 2018
: (4) Unit 2 train A 2B53 switchgear room, Fire Area B, Zone 2091-BB, on November 22, 2018
: (5) Unit 1 north emergency diesel generator room, Fire Area D, Zone 86-G, on November 27, 2018
: (5) Unit 1 north emergency diesel generator room, Fire Area D, Zone 86-G, on November 27, 2018
: (6) Unit 1 east (B) decay heat removal pump room, Fire Area A, Zone 10-EE, on November 28, 2018
: (6) Unit 1 east (B) decay heat removal pump room, Fire Area A, Zone 10-EE, on November 28, 2018  


===71111.07Heat Sink Performance Heat Sink ===
===71111.07Heat Sink Performance Heat Sink===
{{IP sample|IP=IP 71111.07|count=1}}
{{IP sample|IP=IP 71111.07|count=1}}
The inspectors evaluated Unit 2 reactor building containment coolers 2VCC-2A/B/C/D performance on December 17, 2018.
The inspectors evaluated Unit 2 reactor building containment coolers 2VCC-2A/B/C/D performance on December 17, 2018.


===71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification ===
===71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification===
{{IP sample|IP=IP 71111.11|count=1}}
{{IP sample|IP=IP 71111.11|count=1}}
The inspectors observed and evaluated Unit 1 licensed operator requalification scenario on November 27, 2018.
The inspectors observed and evaluated Unit 1 licensed operator requalification scenario on November 27, 2018.


Operator Performance (2 Samples)===
===Operator Performance (2 Samples)===
The inspectors observed and evaluated:
The inspectors observed and evaluated:
: (1) Unit 2 reactor plant startup from Refueling Outage 2R26 on November 19, 2018
: (2) Unit 1 turbine stop valve testing on November 29, 2018


===(1) Unit 2 reactor plant startup from Refueling Outage 2R26 on November 19, 2018
===71111.12Maintenance Effectiveness Routine Maintenance Effectiveness===
: (2) Unit 1 turbine stop valve testing on November 29, 2018
 
===71111.12Maintenance Effectiveness Routine Maintenance Effectiveness ===
{{IP sample|IP=IP 71111.12|count=1}}
{{IP sample|IP=IP 71111.12|count=1}}
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety-significant functions:
The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety-significant functions:
: (1) Unit 1 and Unit 2 50.65(a)(3) periodic evaluation on December 10, 2018 Quality Control (1 Sample)===
: (1) Unit 1 and Unit 2 50.65(a)(3) periodic evaluation on December 10, 2018  
The inspectors evaluated maintenance and quality control activities associated with the


===following equipment performance issues:
===Quality Control (1 Sample)===
: (1) Unit 2 control element assembly CEA-5 capacitor replacement on December 10, 2018
The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues:
: (1) Unit 2 control element assembly CEA-5 capacitor replacement on December 10, 2018  


===71111.13Maintenance Risk Assessments and Emergent Work Control ===
===71111.13Maintenance Risk Assessments and Emergent Work Control===
{{IP sample|IP=IP 71111.13|count=4}}
{{IP sample|IP=IP 71111.13|count=4}}
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
The inspectors evaluated the risk assessments for the following planned and emergent work activities:
Line 118: Line 157:
: (2) Unit 2 plant protective system maintenance activities on October 31, 2018
: (2) Unit 2 plant protective system maintenance activities on October 31, 2018
: (3) Unit 1 and Unit 2 stator heavy lift from onsite storage area to the barge on November 13, 2018
: (3) Unit 1 and Unit 2 stator heavy lift from onsite storage area to the barge on November 13, 2018
: (4) Unit 1 emergent work for the loss of the train A non-vital 4160 volt bus A1 troubleshooting and repair on December 18, 2018
: (4) Unit 1 emergent work for the loss of the train A non-vital 4160 volt bus A1 troubleshooting and repair on December 18, 2018  


===71111.15Operability Determinations and Functionality Assessments ===
===71111.15Operability Determinations and Functionality Assessments===
{{IP sample|IP=IP 71111.15|count=3}}
{{IP sample|IP=IP 71111.15|count=3}}
The inspectors evaluated the following operability determinations and functionality assessments:
The inspectors evaluated the following operability determinations and functionality assessments:
: (1) Unit 2 reactor coolant system thermal sleeves operability assessment on November 2, 2018
: (1) Unit 2 reactor coolant system thermal sleeves operability assessment on November 2, 2018
: (2) Unit 2 reactor vessel monitoring level system detector (RadCal) operability assessment on November 26, 2018
: (2) Unit 2 reactor vessel monitoring level system detector (RadCal) operability assessment on November 26, 2018
: (3) Unit 1 sodium hydroxide spray additive system tank pitting below minimum wall thickness operability assessment on December 12, 2018
: (3) Unit 1 sodium hydroxide spray additive system tank pitting below minimum wall thickness operability assessment on December 12, 2018  


===71111.18Plant Modifications ===
===71111.18Plant Modifications===
{{IP sample|IP=IP 71111.18|count=2}}
{{IP sample|IP=IP 71111.18|count=2}}
The inspectors evaluated the following permanent modifications:
The inspectors evaluated the following permanent modifications:
: (1) Unit 2 control element assembly upper gripper coil stack replacements on October 26, 2018
: (1) Unit 2 control element assembly upper gripper coil stack replacements on October 26, 2018
: (2) Unit 2 removal of timing uncertainty from the control element assembly drop time test on December 31, 2018
: (2) Unit 2 removal of timing uncertainty from the control element assembly drop time test on December 31, 2018  


===71111.19Post Maintenance Testing ===
===71111.19Post Maintenance Testing===
{{IP sample|IP=IP 71111.19|count=7}}
{{IP sample|IP=IP 71111.19|count=7}}
The inspectors evaluated the following post-maintenance tests:
The inspectors evaluated the following post-maintenance tests:
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: (5) Unit 2 check valve 2SI-14A inspection due to valve chattering on November 27, 2018
: (5) Unit 2 check valve 2SI-14A inspection due to valve chattering on November 27, 2018
: (6) Unit 1 main feedwater block isolation valves repair on December 18, 2018
: (6) Unit 1 main feedwater block isolation valves repair on December 18, 2018
: (7) Unit 2 restoration of lifted electrical leads during integrated safeguards testing on December 31, 2018
: (7) Unit 2 restoration of lifted electrical leads during integrated safeguards testing on December 31, 2018  


===71111.20Refueling and Other Outage Activities ===
===71111.20Refueling and Other Outage Activities===
{{IP sample|IP=IP 71111.20|count=2}}
{{IP sample|IP=IP 71111.20|count=2}}
: (1) The inspectors evaluated Unit 2 Refueling Outage 2R26 activities from September 29 to November 2, 2018.
: (1) The inspectors evaluated Unit 2 Refueling Outage 2R26 activities from September 29 to November 2, 2018.
Line 150: Line 189:


===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests:
===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests:
Routine ===
Routine===
{{IP sample|IP=IP 71111.22|count=6}}
{{IP sample|IP=IP 71111.22|count=6}}
: (1) Unit 2 reactor vessel foreign object search and retrieval on October 23, 2018
: (1) Unit 2 reactor vessel foreign object search and retrieval on October 23, 2018
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: (4) Unit 2 as-found local leak-rate test for valve 2CV-5255-1 on November 16, 2018
: (4) Unit 2 as-found local leak-rate test for valve 2CV-5255-1 on November 16, 2018
: (5) Unit 2 integrated safety system testing on November 16, 2018
: (5) Unit 2 integrated safety system testing on November 16, 2018
: (6) Unit 2 emergency feedwater check valves 2EFW-28, 29, 30, and 31, on December 14, 2018
: (6) Unit 2 emergency feedwater check valves 2EFW-28, 29, 30, and 31, on December 14, 2018  


===71114.04Emergency Action Level and Emergency Plan Changes ===
===71114.04Emergency Action Level and Emergency Plan Changes===
{{IP sample|IP=IP 71114.04|count=1}}
{{IP sample|IP=IP 71114.04|count=1}}
The licensee submitted a summary of Emergency Action Level classification procedure changes (Revision 57) to the NRC on October 4, 2018. The inspector conducted an in-office review of the changes from December 4, 2018, to December 14, 2018. This evaluation does not constitute NRC approval.
The licensee submitted a summary of Emergency Action Level classification procedure changes (Revision 57) to the NRC on October 4, 2018. The inspector conducted an in-office review of the changes from December 4, 2018, to December 14, 2018. This evaluation does not constitute NRC approval.


==OTHER ACTIVITIES - BASELINE==
==OTHER ACTIVITIES - BASELINE==
 
===71151Performance Indicator Verification===
===71151Performance Indicator Verification ===
{{IP sample|IP=IP 71151|count=4}}
{{IP sample|IP=IP 71151|count=4}}
The inspectors verified licensee performance indicators submittals listed below:
The inspectors verified licensee performance indicators submittals listed below:
: (1) MS09: Unit 1 and Unit 2 Residual Heat Removal Systems (10/01/2017-09/30/2018)
: (1) MS09: Unit 1 and Unit 2 Residual Heat Removal Systems (10/01/2017-09/30/2018)
: (2) MS10: Unit 1 and Unit 2 Cooling Water Support Systems (10/01/2017-09/30/2018)
: (2) MS10: Unit 1 and Unit 2 Cooling Water Support Systems (10/01/2017-09/30/2018)  


===71152Problem Identification and Resolution Semiannual Trend Review ===
===71152Problem Identification and Resolution Semiannual Trend Review===
{{IP sample|IP=IP 71152|count=2}}
{{IP sample|IP=IP 71152|count=2}}
The inspectors reviewed the licensees corrective action program for trends that might be indicative of more significant safety issues:
The inspectors reviewed the licensees corrective action program for trends that might be indicative of more significant safety issues:
: (1) Procedural quality involving the adequacy of surveillance testing acceptance criteria and testing methodology
: (1) Procedural quality involving the adequacy of surveillance testing acceptance criteria and testing methodology
: (2) Common cause analysis of the ANO Unit 1 Refueling Outage 1R27 human performance issues, Condition Report CR-ANO-C-2018-02728 Annual Follow-up of Selected Issues (1 Sample)===
: (2) Common cause analysis of the ANO Unit 1 Refueling Outage 1R27 human performance issues, Condition Report CR-ANO-C-2018-02728  
The inspectors reviewed the licensees implementation of its corrective action program


===related to the following issues:
===Annual Follow-up of Selected Issues (1 Sample)===
: (1) Unit 2 failure of train A safety-related 4160 volt breaker 2A-303 to automatically close and service water pump B to start during surveillance testing on December 17, 2018
The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:
: (1) Unit 2 failure of train A safety-related 4160 volt breaker 2A-303 to automatically close and service water pump B to start during surveillance testing on December 17, 2018  


===71153Follow-up of Events and Notices of Enforcement Discretion Events ===
===71153Follow-up of Events and Notices of Enforcement Discretion Events===
{{IP sample|IP=IP 71153|count=2}}
{{IP sample|IP=IP 71153|count=2}}
: (1) Unit 2 steam dump and bypass control system malfunction that caused an atmospheric dump valve to open and steam to enter the train A vital 4160 volt switchgear room on November 16, 2018
: (1) Unit 2 steam dump and bypass control system malfunction that caused an atmospheric dump valve to open and steam to enter the train A vital 4160 volt switchgear room on November 16, 2018
: (2) Unit 1 automatic reactor trip due to the loss of the train A non-vital 4160 volt bus A1 on December 18, 2018 Licensee Event Reports (3 Samples)===
: (2) Unit 1 automatic reactor trip due to the loss of the train A non-vital 4160 volt bus A1 on December 18, 2018  
 
===Licensee Event Reports (3 Samples)===
The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:
: (1) Licensee Event Report 0500313/2016-003-01, Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1, on December 10, 2018
: (1) Licensee Event Report 0500313/2016-003-01, Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1, on December 10, 2018
: (2) Licensee Event Report 0500368/2017-001-00, Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions, on December 10, 2018
: (2) Licensee Event Report 0500368/2017-001-00, Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions, on December 10, 2018
: (3) Licensee Event Report 05000313/2018-002-01, Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld, on November 16, 2018
: (3) Licensee Event Report 05000313/2018-002-01, Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld, on November 16,


==INSPECTION RESULTS==
==INSPECTION RESULTS==
Failure to Fully Implement Vendor Manual Recommended Preventative Maintenance Cornerstone             Significance                             Cross-cutting     Inspection Aspect            Procedure Mitigating Systems Green                                         None
Failure to Fully Implement Vendor Manual Recommended Preventative Maintenance Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000368/2018004-01 Closed None


==71152 - NCV 05000368/2018004-01==
==71152 - Problem==
Problem Closed                                                      Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment.
Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment.


Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing.
Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing.
Line 235: Line 275:
Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy, because it was very low safety significance (Green)and was entered into the licensees corrective action program as Condition Reports CR-ANO-2-2018-03442, CR-ANO-2-2018-03454, and CR-ANO-2-2018-03750.
Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy, because it was very low safety significance (Green)and was entered into the licensees corrective action program as Condition Reports CR-ANO-2-2018-03442, CR-ANO-2-2018-03454, and CR-ANO-2-2018-03750.


==71152 - Observation==
Observation
Problem Identification and Resolution Semiannual Trend Review The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site.
 
==71152 - Problem==
Identification and Resolution Semiannual Trend Review The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site.


The NRC inspectors identified a possible trend associated with the surveillance testing methodology and acceptance criteria. Examples included:
The NRC inspectors identified a possible trend associated with the surveillance testing methodology and acceptance criteria. Examples included:
Line 242: Line 284:
* CR-ANO-1-2018-04304. The inspectors identified that Unit 1 Procedure OP-1104.036, Emergency Diesel Generator Operation, Revision 78, did not establish an acceptance criteria for check valve closure testing of diesel starting isolation check valves FO-54A1, FO-55A1, FO-54B1, and FO-55B1. Specifically, the licensee did not determine the maximum allowed check valve leakage to maintain diesel starting air system operability. The licensees corrective action was to determine the appropriate acceptance criteria to assure the valves are, in fact, closed. The licensee and the inspectors validated that the previous test results did not impact diesel starting air system operability.
* CR-ANO-1-2018-04304. The inspectors identified that Unit 1 Procedure OP-1104.036, Emergency Diesel Generator Operation, Revision 78, did not establish an acceptance criteria for check valve closure testing of diesel starting isolation check valves FO-54A1, FO-55A1, FO-54B1, and FO-55B1. Specifically, the licensee did not determine the maximum allowed check valve leakage to maintain diesel starting air system operability. The licensees corrective action was to determine the appropriate acceptance criteria to assure the valves are, in fact, closed. The licensee and the inspectors validated that the previous test results did not impact diesel starting air system operability.
* CR-ANO-C-2018-04296. The inspectors identified a minor violation of Unit 1 TS 5.4.1.a and Unit 2 TS 6.4.1.a for the licensees failure to maintain Unit 1 and Unit 2 Procedure OP-1305.037, Unit 1 Reactor Building Access and Ventilation Leak Rate Testing, Revision 9, and OP-2305.017, Local Leak Rate Testing, Revision 36, respectively. Specifically, the licensee failed to translate Unit 1 TS 5.5.16 and Unit 2 TS 6.5.16 reactor building air lock operability limits as the acceptance criteria into procedures. The licensees corrective actions where to initiate PIFs to translate the TS operability limits as acceptance criteria into the respective procedure.
* CR-ANO-C-2018-04296. The inspectors identified a minor violation of Unit 1 TS 5.4.1.a and Unit 2 TS 6.4.1.a for the licensees failure to maintain Unit 1 and Unit 2 Procedure OP-1305.037, Unit 1 Reactor Building Access and Ventilation Leak Rate Testing, Revision 9, and OP-2305.017, Local Leak Rate Testing, Revision 36, respectively. Specifically, the licensee failed to translate Unit 1 TS 5.5.16 and Unit 2 TS 6.5.16 reactor building air lock operability limits as the acceptance criteria into procedures. The licensees corrective actions where to initiate PIFs to translate the TS operability limits as acceptance criteria into the respective procedure.
* CR-ANO-2-2018-04357. The inspectors identified that Unit 2 Procedure OP-2106.006, Emergency Feedwater System Operations, Revision 98, testing methodology was not in accordance ASME code requirements and did not contain appropriate acceptance criteria for auxiliary feedwater to loop A/B emergency feedwater check valves 2EFW-28, 29, 30, and 31. Specifically, the acceptance criteria for the check valves was if downstream pressure was less than 10 psig or pressure was decreasing, record leakage as zero. The licensees corrective actions are:
* CR-ANO-2-2018-04357. The inspectors identified that Unit 2 Procedure OP-2106.006, Emergency Feedwater System Operations, Revision 98, testing methodology was not in accordance ASME code requirements and did not contain appropriate acceptance criteria for auxiliary feedwater to loop A/B emergency feedwater check valves 2EFW-28, 29, 30, and 31. Specifically, the acceptance criteria for the check valves was if downstream pressure was less than 10 psig or pressure was decreasing, record leakage as zero. The licensees corrective actions are:  
1. Determine the design basis allowed leakage for valves 2EFW-28, 29, 30, and 31 and update the procedure and design basis documents.


2. Initiate a PIF to update the procedure to incorporate appropriate testing methods.
===1. Determine the design basis allowed leakage for valves 2EFW-28, 29, 30, and 31===
and update the procedure and design basis documents.


===2. Initiate a PIF to update the procedure to incorporate appropriate testing methods.===
In response to the inspectors observations, the licensee entered this trend into their corrective action program for resolution as Condition Report CR-ANO-C-2019-00033.
In response to the inspectors observations, the licensee entered this trend into their corrective action program for resolution as Condition Report CR-ANO-C-2019-00033.


Line 252: Line 295:


==71152 - Problem==
==71152 - Problem==
Identification and Resolution Semiannual Trend Review


Identification and Resolution Semiannual Trend Review The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site.
The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site.
 
The inspectors reviewed the corrective action program documentation associated with the common cause analysis of the ANO Unit 1 Refueling Outage 1R27 performance issues, documented in Condition Report CR-ANO-C-2018-02728. The inspectors identified 12 documented human performance errors that caused events, rework, and delays. The licensee initiated the condition report following these events in an effort to document and discover how to prevent these issues from continuing to occur. The licensee identified five causal factors and developed a corrective action for each:


The inspectors reviewed the corrective action program documentation associated with the common cause analysis of the ANO Unit 1 Refueling Outage 1R27 performance issues, documented in Condition Report CR-ANO-C-2018-02728. The inspectors identified 12 documented human performance errors that caused events, rework, and delays. The licensee initiated the condition report following these events in an effort to document and discover how to prevent these issues from continuing to occur. The licensee identified five causal factors and developed a corrective action for each:
===1. Insufficient ownership and accountability by licensee and supplemental personnel===
1. Insufficient ownership and accountability by licensee and supplemental personnel resulted in a tolerance of low standards in sustaining nuclear professional behaviors by individual contributors and leadership. Corrective Action (CA) included:
resulted in a tolerance of low standards in sustaining nuclear professional behaviors by individual contributors and leadership. Corrective Action (CA) included:
* Integrate the Own It Accountability Model in work preparation/execution activities into the licensees work preparation meetings to improve ownership and accountability in the pursuit of excellence for licensee work preparation and execution.
* Integrate the Own It Accountability Model in work preparation/execution activities into the licensees work preparation meetings to improve ownership and accountability in the pursuit of excellence for licensee work preparation and execution.
* Implement a licensee Organization Effectiveness Top Issues List and use the organization effectiveness model, administrative tools, and communications media forums to keep issues visible and track to resolution.
* Implement a licensee Organization Effectiveness Top Issues List and use the organization effectiveness model, administrative tools, and communications media forums to keep issues visible and track to resolution.
Line 264: Line 310:


===2. Management and peer coaching did not consistently correct unacceptable behaviors===
===2. Management and peer coaching did not consistently correct unacceptable behaviors===
due to the tendency of some leaders to avoid conflict and difficult conversions.
due to the tendency of some leaders to avoid conflict and difficult conversions.


Line 276: Line 321:


===3. Licensee personal became complacent to the requirements for strict adherence to===
===3. Licensee personal became complacent to the requirements for strict adherence to===
procedures and work instructions due to the lack of immediate consequence for noncompliance. Corrective actions included:
procedures and work instructions due to the lack of immediate consequence for noncompliance. Corrective actions included:
* Implement remediation model for procedure/work instruction adherence. The intent of this action was to provide clear management expectations and accountability at all levels of the organization for procedure and work instruction adherence.
* Implement remediation model for procedure/work instruction adherence. The intent of this action was to provide clear management expectations and accountability at all levels of the organization for procedure and work instruction adherence.
* Incorporate Procedure EN-HU-106, Procedure and Work Instructions Use and Adherence, Revision 7, training into maintenance continuing training.
* Incorporate Procedure EN-HU-106, Procedure and Work Instructions Use and Adherence, Revision 7, training into maintenance continuing training.


4. Risk was not always recognized or was inappropriately accepted by individuals without sufficient leadership engagement in real time decision-making. Corrective actions included:
===4. Risk was not always recognized or was inappropriately accepted by individuals without===
* 2R26 standards team focus on real-time decision-making (stop when unsure).
sufficient leadership engagement in real time decision-making. Corrective actions included:  
*  
{{a|2R26}}


==2R26 standards team focus on real-time decision-making (stop when unsure).
==
The intent of this action was to ensure the 2R26 standards team plan included a focus area for field observations related to stop when unsure (real-time decision making) and pre-job briefs (work preparation, roles and responsibilities, and risk mitigation).
The intent of this action was to ensure the 2R26 standards team plan included a focus area for field observations related to stop when unsure (real-time decision making) and pre-job briefs (work preparation, roles and responsibilities, and risk mitigation).
* 2R26 personnel briefing on unknowingly accepting station risk. The intent of this action was to provide communication to 2R26 works to increase the awareness of unknowingly making decisions in the field that may increase station risk.


5. Licensee leadership did not consistently manage and control outage work scope which impacted the stations ability to effectively prepare and execute scheduled work activities. Corrective actions included:
*
 
{{a|2R26}}
 
==2R26 personnel briefing on unknowingly accepting station risk. The intent of==
this action was to provide communication to 2R26 works to increase the awareness of unknowingly making decisions in the field that may increase station risk.
 
===5. Licensee leadership did not consistently manage and control outage work scope which===
impacted the stations ability to effectively prepare and execute scheduled work activities. Corrective actions included:
* Validate effective change management when 2R26 major work was reassigned near the outage. The intent of this action was to provide effective change management for scoping transitions that occur within 60 days of schedule start date for 2R26.
* Validate effective change management when 2R26 major work was reassigned near the outage. The intent of this action was to provide effective change management for scoping transitions that occur within 60 days of schedule start date for 2R26.
* Establish unit specific outage work scope priority lists. The intent of this action was clearly defined outage work scope priorities and to control the combined outage work scope within budgeted resources and margins to allow adequate time for work preparation and execution using the prevention model.
* Establish unit specific outage work scope priority lists. The intent of this action was clearly defined outage work scope priorities and to control the combined outage work scope within budgeted resources and margins to allow adequate time for work preparation and execution using the prevention model.
Line 303: Line 359:
71111.04 - Equipment Alignment
71111.04 - Equipment Alignment
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
1-2012-00362       1-2012-00363       1-2018-04976   C-2016-01706
1-2012-00362
1-2012-00363
1-2018-04976
C-2016-01706  
 
Procedures
Procedures
Number             Title                                           Revision
Number
OP-1104.002       Makeup and Purification System Operation       95
Title
OP-1106.006       Emergency Feedwater Operations                 101
Revision
OP-1107.001       Electrical System Operations                   120
OP-1104.002
OP-2106.006       Emergency Feedwater Operations                 99
Makeup and Purification System Operation
OP-1106.006
Emergency Feedwater Operations
101
OP-1107.001
Electrical System Operations
20
OP-2106.006
Emergency Feedwater Operations  
 
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title                                           Revision
Number  
EC-65360           CALC-82-D-2086-01 Mark Up to Account for       0
 
Title  
 
Revision
EC-65360
CALC-82-D-2086-01 Mark Up to Account for
Condensate Lost due to Pump Bearing and Correct
Condensate Lost due to Pump Bearing and Correct
Computation Error
Computation Error  
 
Calculations
Calculations
Number             Title                                           Revision
Number
CALC-82-D-2086- Volume of CST T-41B Requiring Tornado Missile     4
Title
Protection
Revision
CALC-82-D-2086-
Volume of CST T-41B Requiring Tornado Missile
Protection  
 
71111.05 - Fire Protection
71111.05 - Fire Protection
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
2-2018-04226
2-2018-04226  
 
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title
Number  
1A-372-86-G       Unit 1 Plant Fire Protection
 
1B-317-10-EE       Unit 1 Plant Fire Protection
Title  
1B-335-38-Y       Unit 1 Plant Fire Protection
 
2A-404-2151-A     Unit 2 Plant Fire Protection
1A-372-86-G
Unit 1 Plant Fire Protection
1B-317-10-EE
Unit 1 Plant Fire Protection
1B-335-38-Y
Unit 1 Plant Fire Protection
2A-404-2151-A
Unit 2 Plant Fire Protection  
 
71111.07 - Heat Sink Performance
71111.07 - Heat Sink Performance
Work Orders
Work Orders
503112       52675121      52769910      52770785  52770786
503112
2675121
2769910
2770785
2770786
 
Procedures
Procedures
Number             Title                                                 Revision
Number
OP-2305.062       Service Water System Flow Testing                     2
Title
Revision
OP-2305.062
Service Water System Flow Testing  
 
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title                                                 Revision
Number  
EC-72776           Document the Results of the 2R25 As-Left Service       0
 
Water Flow Test
Title  
 
Revision
EC-72776
Document the Results of the 2R25 As-Left Service
Water Flow Test  
 
Calculations
Calculations
Number             Title                                                 Revision
Number
CALC-88-E-0032-   Unit 2 Containment Service Water Cooling Coils Thermal 3
Title
Revision
CALC-88-E-0032-
Unit 2 Containment Service Water Cooling Coils Thermal
Performance
Performance
CALC-91-R-2013-   Service Water Performance Testing Methodology         28
CALC-91-R-2013-
CALC-99-E-0033-   ANO-2 Containment Cooler Fan Motor Horsepower         0
Service Water Performance Testing Methodology
CALC-99-E-0033-
ANO-2 Containment Cooler Fan Motor Horsepower
during a DBA Under Uprate Conditions
during a DBA Under Uprate Conditions
CALC-             Determination of Error Associated with Air Flow       0
CALC-
991522E201-01      Measurements of Reactor Building Containment Coolers
991522E201-01
Determination of Error Associated with Air Flow
Measurements of Reactor Building Containment Coolers  
 
71111.11 - Licensed Operator Requalification Program
71111.11 - Licensed Operator Requalification Program
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title                                                 Revision
Number  
A1SXMLOR1902       Unit 1 Licensed Operation Requalification Scenario     0
 
Title  
 
Revision
A1SXMLOR1902
Unit 1 Licensed Operation Requalification Scenario  
 
71111.12 -Maintenance Effectiveness
71111.12 -Maintenance Effectiveness
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
C-2018-03631
C-2018-03631  
 
Work Orders
Work Orders
00486027
00486027  
 
Procedures
Procedures
Number             Title                                                 Revision
Number
EN-DC-207         Maintenance Rule Periodic Assessment                   3
Title
Revision
EN-DC-207
Maintenance Rule Periodic Assessment  
 
Drawings
Drawings
Number             Title
Number
E-2258             Schematic Diagram Reactor Control Element Assembly
Title
M-2001-L1-196     CEDMCS Schematic Diagram Subgroup Filter Panel
E-2258
Schematic Diagram Reactor Control Element Assembly
M-2001-L1-196
CEDMCS Schematic Diagram Subgroup Filter Panel  
 
Calculations
Calculations
Number             Title                                                   Revision
Number
CALC-ANOC-SE-     Maintenance Rule 10 CFR 50.65(a)(3) Periodic             0
Title
17-00001          Assessment January 1, 2016, to June 30, 2017
Revision
CALC-ANOC-SE-
17-00001
Maintenance Rule 10 CFR 50.65(a)(3) Periodic
Assessment January 1, 2016, to June 30, 2017  
 
71111.13 - Maintenance Risk Assessments and Emergent Work Control
71111.13 - Maintenance Risk Assessments and Emergent Work Control
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
2-2018-02847       2-2018-02909
2-2018-02847
2-2018-02909  
 
Procedures
Procedures
Number             Title                                                   Revision
Number
2102.010           Plant Cooldown                                           57
Title
Revision
2102.010
Plant Cooldown  
 
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title                                                   Revision
Number  
NUREG 1022         Event Report Guidelines 10 CFR 50.72 and 50.73           3
 
Title  
 
Revision
NUREG 1022
Event Report Guidelines 10 CFR 50.72 and 50.73  
 
71111.15 - Operability Determinations and Functionality Assessments
71111.15 - Operability Determinations and Functionality Assessments
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
1-2015-02718       1-2018-04619       1-2018-04636       1-2018-04668     1-2018-04671
1-2015-02718
1-2018-04674       2-2013-01190       2-2018-02976       2-2018-03127     2-2018-03252
1-2018-04619
2-2018-03304
1-2018-04636
1-2018-04668
1-2018-04671
1-2018-04674
2-2013-01190
2-2018-02976
2-2018-03127
2-2018-03252
2-2018-03304  
 
Procedures
Procedures
Number             Title                                                   Revision
Number
EN-OP-104         Operability Determination Process                       16
Title
Revision
EN-OP-104
Operability Determination Process  
 
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title                                                   Date
Number  
EC-79912           Engineering Change
 
EC-80182           Engineering Change
Title  
EC-79906           Engineering Change
 
N-705             Evaluation Criteria for Temporary Acceptance of         October 12,
Date
Degradation in Moderate Energy Class 2 or 3 Vessels     2006
EC-79912
Engineering Change
EC-80182
Engineering Change
EC-79906
Engineering Change
N-705
Evaluation Criteria for Temporary Acceptance of
Degradation in Moderate Energy Class 2 or 3 Vessels
and Tanks
and Tanks
October 12,
2006
Calculations
Calculations
Number             Title                                                   Revision
Number
CALC-ANO2-ME-     Evaluation of Safety Injection Nozzles and Thermal       0
Title
18-00003          Sleeves Supporting Justification for Continued Operation
Revision
at ANO2
CALC-ANO2-ME-
18-00003
Evaluation of Safety Injection Nozzles and Thermal
Sleeves Supporting Justification for Continued Operation
at ANO2  
 
Calculations
Calculations
Number             Title                                                   Revision
Number
CALC-ANO2-ME-     Operability Assessment for Primary Side Loose Parts     0
Title
18-00004          from Migration of Safety Injection Nozzle Thermal Sleeve
Revision
at Arkansas Nuclear One Unit 2
CALC-ANO2-ME-
18-00004
Operability Assessment for Primary Side Loose Parts
from Migration of Safety Injection Nozzle Thermal Sleeve
at Arkansas Nuclear One Unit 2  
 
71111.18 - Plant Modifications
71111.18 - Plant Modifications
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
2-2018-04166
2-2018-04166  
 
Work Orders
Work Orders
471461       512940        52790774
471461
2940
2790774
 
Procedures
Procedures
Number             Title                                                   Revision
Number
OP-2302.046       CEA Drop Time Test                                       17
Title
ULD-2-SYS-36       Control Element Drive Mechanism                         2
Revision
OP-2302.046
CEA Drop Time Test
ULD-2-SYS-36
Control Element Drive Mechanism  
 
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title                                                   Revision
Number  
EC-75702           Replace CEA Upper Gripper Coils with Westinghouse       0
 
Title  
 
Revision
EC-75702
Replace CEA Upper Gripper Coils with Westinghouse
High Temp Coils
High Temp Coils
EC-78985           Amend Low Voltage Setting for HT Upper Gripper Coils     0
EC-78985
EC-80516           ANO-2 CEA Drop Time Uncertainty Relaxation               0
Amend Low Voltage Setting for HT Upper Gripper Coils
EC-80516
ANO-2 CEA Drop Time Uncertainty Relaxation  
 
71111.19 - Post Maintenance Testing
71111.19 - Post Maintenance Testing
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
1-2018-05315       1-2018-05328       1-2018-05350       2-2018-02213     2-2018-03919
1-2018-05315
2-2018-04002       2-2018-04166       2-2018-04446
1-2018-05328
1-2018-05350
2-2018-02213
2-2018-03919
2-2018-04002
2-2018-04166
2-2018-04446  
 
Work Orders
Work Orders
2399       486741       509778       512499        512940      52573102    52776588
2399
2790774     52805699
486741
509778
2499
2940
2573102
2776588
2790774
2805699
 
Procedures
Procedures
Number             Title                                                   Revision
Number
OP-2102.001       Plant Pre-heatup and Pre-critical Checklist             91
Title
OP-2302.046       CEA Drop Time Test                                       17
Revision
OP-2305.001       Integrated Engineering Safeguards Test                   32
OP-2102.001
OP-2305.017       Local Leak Rate Testing                                 36
Plant Pre-heatup and Pre-critical Checklist
OP-2302.046
CEA Drop Time Test
OP-2305.001
Integrated Engineering Safeguards Test
OP-2305.017
Local Leak Rate Testing  
 
71111.20 - Refueling and Other Outage Activities
71111.20 - Refueling and Other Outage Activities
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
1-2018-05325       2-2018-02129       2-2018-02130       C-2018-04030
1-2018-05325
2-2018-02129
2-2018-02130
C-2018-04030  
 
Work Orders
Work Orders
2770782
2770782  
 
Procedure
Procedure
Number             Title                                                   Revision
Number
OP-2306.024       Unit 2 (IST) Relief Valve Setpoint Testing             25
Title
OP-2505.004       Unit 2 Core Support Barrel Removal                     11
Revision
OP-2306.024
Unit 2 (IST) Relief Valve Setpoint Testing
OP-2505.004
Unit 2 Core Support Barrel Removal  
 
71111.22 - Surveillance Testing
71111.22 - Surveillance Testing
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
1-2018-00963       1-2018-04790       1-2018-04795       1-2018-04975     2-2004-01688
1-2018-00963
2-2018-04357       C-2018-04296       C-2018-04339
1-2018-04790
1-2018-04795
1-2018-04975
2-2004-01688
2-2018-04357
C-2018-04296
C-2018-04339  
 
Work Orders
Work Orders
486741       52573102      52719205      52764513    52770817    52771820    52780270
486741
2815431
2573102
2719205
2764513
2770817
2771820
2780270
2815431  
 
Procedures
Procedures
Number             Title                                                   Revision
Number
ER-ANO-2006-       U2 EFW Alignment to QCST Evaluation                    0
Title
Revision
ER-ANO-2006-
0389-000
0389-000
OP-1305.037       Unit 1 Reactor Building Access and Ventilation Leak     9 (8)
U2 EFW Alignment to QCST Evaluation
Rate Testing
OP-1305.037
OP-2106.006       Emergency Feedwater System Operation                   98
Unit 1 Reactor Building Access and Ventilation Leak
OP-2305.001       Integrated Engineering Safeguards Test                 32
Rate Testing
OP-2305.017       Local Leak Rate Testing                                 36
(8)
SEP-ANO-2-IST-1 Inservice Testing Bases Document                           4
OP-2106.006
SEP-APJ-002       Arkansas Nuclear One Containment Leakage Rate           7
Emergency Feedwater System Operation
OP-2305.001
Integrated Engineering Safeguards Test
OP-2305.017
Local Leak Rate Testing
SEP-ANO-2-IST-1 Inservice Testing Bases Document
SEP-APJ-002
Arkansas Nuclear One Containment Leakage Rate
Testing (Appendix J)
Testing (Appendix J)
ULD-2-SYS-12       Emergency Feedwater System                             11
ULD-2-SYS-12
Emergency Feedwater System  
 
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title                                                   Revision
Number  
M-2204, Sheet     Emergency Feedwater                                    74
 
Title  
 
Revision
M-2204, Sheet
P&ID
P&ID
Emergency Feedwater
Calculations
Calculations
Number             Title                                                 Revision
Number
CALC-00-E-0010-   Appendix J Containment Maximum Allowable Leakage     0
Title
Revision
CALC-00-E-0010-
Appendix J Containment Maximum Allowable Leakage
Rate (La)
Rate (La)
CALC-00-E-0023-   Unit 1 Appendix J Containment Maximum Allowable       0
CALC-00-E-0023-
Unit 1 Appendix J Containment Maximum Allowable
Leakage Rate (La)
Leakage Rate (La)
CALC-89-D-2043-   Failure Modes Effect Analysis for the Addition of the 0
CALC-89-D-2043-
Auxiliary Feedwater Pump
Failure Modes Effect Analysis for the Addition of the
Auxiliary Feedwater Pump  
 
71114.04 - Emergency Action Level and Emergency Plan Changes
71114.04 - Emergency Action Level and Emergency Plan Changes
Procedures
Procedures
Number             Title                                                 Revision
Number
1903.010           Emergency Action Level Classification                 44, 56
Title
Revision
1903.010
Emergency Action Level Classification
44, 56
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title                                                 Date
Number  
0CAN101801         Emergency Plan Implementing Procedure, Arkansas       October 4, 2018
 
Title  
 
Date
0CAN101801
Emergency Plan Implementing Procedure, Arkansas
Nuclear One, Units 1 and 2,
Nuclear One, Units 1 and 2,
Docket Nos. 50-313, 50-368, and 72-13; License
Docket Nos. 50-313, 50-368, and 72-13; License
Nos. DPR-51 and NPF-6
Nos. DPR-51 and NPF-6
October 4, 2018
71151 - Performance Indicator Verification
71151 - Performance Indicator Verification
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
1-2017-03024       1-2018-03729
1-2017-03024
1-2018-03729  
 
Procedures
Procedures
Number             Title                                                 Revision
Number
EN-LI-114         Regulatory Performance Indicator Process             12
Title
Revision
EN-LI-114
Regulatory Performance Indicator Process  
 
Calculations
Calculations
Number             Title                                                 Revision
Number
CALC-ANO1-SA-     ANO-1 Mitigating System Performance Index Basis      1
Title
Revision
CALC-ANO1-SA-
16-00001
16-00001
CALC-ANO2-SA-      ANO-2 Mitigating System Performance Index Basis       3
ANO-1 Mitigating System Performance Index Basis
CALC-ANO2-SA-
06-00001
06-00001
ANO-2 Mitigating System Performance Index Basis
71152 - Problem Identification and Resolution
71152 - Problem Identification and Resolution
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
1-2018-00963       1-2018-04296       1-2018-04790       1-2018-04975   C-2018-04339
1-2018-00963
2-2018-03442       2-2018-03442       2-2018-03454       2-2018-03750   2-2009-02997
1-2018-04296
1-2018-03223       2-2018-01009       1-2018-04304       C-2018-04296   2-2018-04357
1-2018-04790
C-2019-00033
1-2018-04975
C-2018-04339
2-2018-03442
2-2018-03442
2-2018-03454
2-2018-03750
2-2009-02997
1-2018-03223
2-2018-01009
1-2018-04304
C-2018-04296
2-2018-04357
C-2019-00033  
 
Work Orders
Work Orders
411600       511409       52775094
411600
511409
2775094
 
Procedures
Procedures
Number             Title                                                 Revision
Number
OP-1305.037       Unit 1 Reactor Building Access and Ventilation Leak   9 (8)
Title
Rate Testing
Revision
OP-2416.007       Unit 2 - 2A3 Bus Switchgear Inspection                 17
OP-1305.037
Unit 1 Reactor Building Access and Ventilation Leak
Rate Testing
(8)
OP-2416.007
Unit 2 - 2A3 Bus Switchgear Inspection  
 
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title
Number  
PIF 1-18-0125     Procedure Improvement Form for OP-1305.037
 
Title  
 
PIF 1-18-0125
Procedure Improvement Form for OP-1305.037  
 
71153 - Follow-up of Events and Notices of Enforcement Discretion
71153 - Follow-up of Events and Notices of Enforcement Discretion
Condition Reports (CR-ANO-)
Condition Reports (CR-ANO-)
1-2017-00241       1-2018-05311       1-2018-05312       1-2018-05326   1-2018-05332
1-2017-00241
1-2018-05340       1-2018-05360       2-2017-01555       2-2018-04225   2-2018-04226
1-2018-05311
2-2018-04227       2-2018-04230       2-2018-04241       2-2018-04244   2-2018-04336
1-2018-05312
C-2018-04699
1-2018-05326
1-2018-05332
1-2018-05340
1-2018-05360
2-2017-01555
2-2018-04225
2-2018-04226
2-2018-04227
2-2018-04230
2-2018-04241
2-2018-04244
2-2018-04336
C-2018-04699  
 
Procedures
Procedures
Number             Title                                                 Revision
Number
203.012B         Annunciator 2K02 Corrective Action                     45
Title
EN-OP-126         Post Transient Response and Review                     1
Revision
203.012B
Annunciator 2K02 Corrective Action
EN-OP-126
Post Transient Response and Review  
 
Drawings
Drawings
Number             Title                                                 Revision
Number
2HBD-300-1         Small Pipe Isometric Auxiliary Building               7
Title
2HBD-300-2         Small Pipe Isometric Turbine Building                 5
Revision
A-2103             Architectural Floor Plan at el 368, 372, and 374 6 35
2HBD-300-1
A-2104             Architectural Floor Plan at el 386                   36
Small Pipe Isometric Auxiliary Building
A-2114             Architectural Exterior Elevations and Sections         14
2HBD-300-2
E-34               Schematic Meter and Relay Diagram 4160V System,       12
Small Pipe Isometric Turbine Building
A-2103
Architectural Floor Plan at el 368, 372, and 374 6
A-2104
Architectural Floor Plan at el 386
A-2114
Architectural Exterior Elevations and Sections
E-34
Schematic Meter and Relay Diagram 4160V System,
Main Supply
Main Supply
M-2112             Plumbing and Drainage Aux Bldg                         16
M-2112
M-2116             Plumbing and Drainage Aux Bldg                         25
Plumbing and Drainage Aux Bldg
M-2116
Plumbing and Drainage Aux Bldg  
 
Miscellaneous
Miscellaneous
Documents
Documents
Number             Title                                                 Revision
Number  
STM 2-15           Steam Generators and Main Steam System                 20
 
STM 2-23           Steam Dump and Bypass Control System                   14
Title  
 
Revision
STM 2-15
Steam Generators and Main Steam System
STM 2-23
Steam Dump and Bypass Control System  


ML19024A075
ML19024A075
SUNSI Review           ADAMS:             Non-Publicly Available     Non-Sensitive Keyword:
SUNSI Review
By: NOKeefe           Yes No         Publicly Available         Sensitive     NRC-002
ADAMS:
OFFICE         SRI:DRP/D       RI:DRP/D       RI:DRP/D         BC:DRS/EB1 ABC:DRS/EB2 BC:DRS/OB
Non-Publicly Available
NAME           CHenderson     MTobin         TSullivan       VGaddy       JDrake       GWerner
Non-Sensitive
SIGNATURE     cmh             MCT           TMS             vgg         JFD           GEW
Keyword:
DATE           1/10/2019       1/10/2019     1/10/2019       1/14/19     1/14/19       01/12/2019
By: NOKeefe
OFFICE         BC:DRS/PSB2 ATL:DRS/IPAT BC:DRP/D
Yes No
NAME           HGepford       RKellar       NOKeefe
Publicly Available
SIGNATURE     hjg             RLK           NFO
Sensitive
DATE           01/14/2019     01/14/2019     1/23/19
NRC-002
OFFICE
SRI:DRP/D
RI:DRP/D
RI:DRP/D
BC:DRS/EB1
ABC:DRS/EB2
BC:DRS/OB
NAME
CHenderson
MTobin
TSullivan
VGaddy
JDrake
GWerner
SIGNATURE
cmh
MCT
TMS
vgg
JFD
GEW
DATE
1/10/2019
1/10/2019
1/10/2019
1/14/19
1/14/19
01/12/2019
OFFICE
BC:DRS/PSB2
ATL:DRS/IPAT
BC:DRP/D  
 
NAME
HGepford
RKellar
NOKeefe  
 
SIGNATURE
hjg
RLK
NFO  
 
DATE
01/14/2019
01/14/2019
1/23/19
}}
}}

Latest revision as of 05:56, 5 January 2025

NRC Integrated Inspection Report 05000313/2018004 and 05000368/2018004
ML19024A075
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 01/23/2019
From: O'Keefe N
NRC/RGN-IV/DRP/RPB-D
To: Richard Anderson
Entergy Operations
References
IR 2018004
Download: ML19024A075 (24)


Text

January 23, 2019

SUBJECT:

ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT 05000313/2018004 AND 05000368/2018004

Dear Mr. Anderson:

On December 31, 2018, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at your Arkansas Nuclear One, Units 1 and 2. On January 3, 2019, the NRC inspectors discussed the results of this inspection with Mr. J. Kirkpatrick, General Manager of Plant Operations, and other members of your staff. The results of this inspection are documented in the enclosed report.

NRC inspectors documented one finding of very low safety significance (Green) in this report.

This finding involved a violation of NRC requirements. The NRC is treating this violation as a non-cited violation (NCV) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violation or significance of this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional Administrator, Region IV; the Director, Office of Enforcement; and the NRC resident inspector at the Arkansas Nuclear One. This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with 10 CFR 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Neil OKeefe, Chief Project Branch D Division of Reactor Projects

Docket Nos. 50-313 and 50-368 License Nos. DPR-51 and NPF-6

Enclosure:

Inspection Report 05000313/2018004 and 05000368/2018004 w/Attachment:

Documents Reviewed

Enclosure U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Number(s):

05000313, 05000368

License Number(s):

DPR-51, NPF-6

Report Number(s):

05000313/2018004, 05000368/2018004

Enterprise Identifier: I-2018-004-0005

Licensee:

Entergy Operations, Inc.

Facility:

Arkansas Nuclear One, Units 1 and 2

Location:

Russellville, Arkansas

Inspection Dates:

October 1, 2018 to December 31, 2018

Inspectors:

C. Henderson, Senior Resident Inspector

M. Tobin, Resident Inspector

T. Sullivan, Resident Inspector

R. Bywater, Project Engineer

J. Dixon, Senior Project Engineer

S. Hedger, Emergency Preparedness Inspector

Approved By:

Neil OKeefe

Branch Chief

Division of Reactor Projects

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Arkansas Nuclear One, Units 1 and 2, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information. A self-revealed violation and additional items are summarized in the tables below.

List of Findings and Violations

Failure to Fully Implement Vendor Manual Recommended Preventive Maintenance Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000368/2018004-01 Closed None 71152 -

Problem Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment.

Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches because only some electrical contacts were being cleaned. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing.

Additional Tracking Items

Type Issue number Title Inspection Procedure Status LER 0500313/2016-003-01

Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1 71153 Closed LER 0500368/2017-001-00 Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions 71153 Closed LER 05000313/2018-002-01 Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld 71153 Closed

PLANT STATUS

Unit 1 began the inspection period at full power. On November 29, 2018, power was lowered to 85 percent to perform main turbine valve testing and was returned to full power.

On December 18, 2018, Unit 1 had an automatic reactor trip from 100 percent power after the loss of power to non-vital 4160 volt bus A1. On December 21, 2018, Unit 1 commenced a reactor startup and the reactor was made critical. The unit was returned to rated thermal power on December 23, 2018.

Unit 2 began the inspection period in shutdown for Refueling Outage 2R26, which started on September 29, 2018. On November 19, 2018, Unit 2 commenced a reactor startup and the reactor was made critical. The unit was returned to full power on November 24,

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs)in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html.

Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed plant status activities described in IMC 2515, Appendix D, Plant Status, and conducted routine reviews using IP 71152, Problem Identification and Resolution. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04Equipment Alignment Partial Walkdown

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 2 train A spent fuel pool cooling during full core offload on November 6, 2018
(2) Unit 2 train A shutdown cooling system on November 10, 2018
(3) Unit 1 train A high pressure injection system on November 21, 2018
(4) Unit 1 and Unit 2 quality condensate storage tank on November 28, 2018
(5) Unit 2 train A plant protective system on December 31, 2018

71111.05AQFire Protection Annual/Quarterly Quarterly Inspection

The inspectors evaluated fire protection program implementation in the following selected areas:

(1) Unit 1 emergency feedwater pump area, Fire Area C, Zone 38-Y, on October 23, 2018
(2) Unit 2 fuel handling area, Fire Area B, Zone 2151-A, on October 23, 2018
(3) Unit 2 train A 2A3 switchgear room, Fire Area II, Zone 2101-AA, on November 22, 2018
(4) Unit 2 train A 2B53 switchgear room, Fire Area B, Zone 2091-BB, on November 22, 2018
(5) Unit 1 north emergency diesel generator room, Fire Area D, Zone 86-G, on November 27, 2018
(6) Unit 1 east (B) decay heat removal pump room, Fire Area A, Zone 10-EE, on November 28, 2018

71111.07Heat Sink Performance Heat Sink

The inspectors evaluated Unit 2 reactor building containment coolers 2VCC-2A/B/C/D performance on December 17, 2018.

71111.11Licensed Operator Requalification Program and Licensed Operator Performance Operator Requalification

The inspectors observed and evaluated Unit 1 licensed operator requalification scenario on November 27, 2018.

Operator Performance (2 Samples)

The inspectors observed and evaluated:

(1) Unit 2 reactor plant startup from Refueling Outage 2R26 on November 19, 2018
(2) Unit 1 turbine stop valve testing on November 29, 2018

71111.12Maintenance Effectiveness Routine Maintenance Effectiveness

The inspectors evaluated the effectiveness of routine maintenance activities associated with the following equipment and/or safety-significant functions:

(1) Unit 1 and Unit 2 50.65(a)(3) periodic evaluation on December 10, 2018

Quality Control (1 Sample)

The inspectors evaluated maintenance and quality control activities associated with the following equipment performance issues:

(1) Unit 2 control element assembly CEA-5 capacitor replacement on December 10, 2018

71111.13Maintenance Risk Assessments and Emergent Work Control

The inspectors evaluated the risk assessments for the following planned and emergent work activities:

(1) Unit 1 Technical Specification 3.0.3 entry for control room emergency air cleanup system when securing Unit 2 emergency diesel generator 2 on October 31, 2018
(2) Unit 2 plant protective system maintenance activities on October 31, 2018
(3) Unit 1 and Unit 2 stator heavy lift from onsite storage area to the barge on November 13, 2018
(4) Unit 1 emergent work for the loss of the train A non-vital 4160 volt bus A1 troubleshooting and repair on December 18, 2018

71111.15Operability Determinations and Functionality Assessments

The inspectors evaluated the following operability determinations and functionality assessments:

(1) Unit 2 reactor coolant system thermal sleeves operability assessment on November 2, 2018
(2) Unit 2 reactor vessel monitoring level system detector (RadCal) operability assessment on November 26, 2018
(3) Unit 1 sodium hydroxide spray additive system tank pitting below minimum wall thickness operability assessment on December 12, 2018

71111.18Plant Modifications

The inspectors evaluated the following permanent modifications:

(1) Unit 2 control element assembly upper gripper coil stack replacements on October 26, 2018
(2) Unit 2 removal of timing uncertainty from the control element assembly drop time test on December 31, 2018

71111.19Post Maintenance Testing

The inspectors evaluated the following post-maintenance tests:

(1) Unit 2 rod drop timing surveillance November 16, 2018
(2) Unit 2 valve 2CV-5255-1 as left local leak-rate test on November 17, 2018
(3) Unit 2 control element assembly CEA-5 capacitor replacement and control element assembly upper gripper coil replacement on November 17, 2018
(4) Unit 2 reactor vessel monitoring level system detector (Radcal) replacement on November 20, 2018
(5) Unit 2 check valve 2SI-14A inspection due to valve chattering on November 27, 2018
(6) Unit 1 main feedwater block isolation valves repair on December 18, 2018
(7) Unit 2 restoration of lifted electrical leads during integrated safeguards testing on December 31, 2018

71111.20Refueling and Other Outage Activities

(1) The inspectors evaluated Unit 2 Refueling Outage 2R26 activities from September 29 to November 2, 2018.
(2) The inspectors evaluated Unit 1 Forced Outage 2018-002 activities from December 18 to December 21, 2018.

===71111.22Surveillance Testing The inspectors evaluated the following surveillance tests:

Routine===

(1) Unit 2 reactor vessel foreign object search and retrieval on October 23, 2018
(2) Unit 1 and Unit 2 personnel airlock door seal leakage testing on October 23, 2018
(3) Unit 2 rod drop testing on November 14, 2018
(4) Unit 2 as-found local leak-rate test for valve 2CV-5255-1 on November 16, 2018
(5) Unit 2 integrated safety system testing on November 16, 2018
(6) Unit 2 emergency feedwater check valves 2EFW-28, 29, 30, and 31, on December 14, 2018

71114.04Emergency Action Level and Emergency Plan Changes

The licensee submitted a summary of Emergency Action Level classification procedure changes (Revision 57) to the NRC on October 4, 2018. The inspector conducted an in-office review of the changes from December 4, 2018, to December 14, 2018. This evaluation does not constitute NRC approval.

OTHER ACTIVITIES - BASELINE

71151Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

(1) MS09: Unit 1 and Unit 2 Residual Heat Removal Systems (10/01/2017-09/30/2018)
(2) MS10: Unit 1 and Unit 2 Cooling Water Support Systems (10/01/2017-09/30/2018)

71152Problem Identification and Resolution Semiannual Trend Review

The inspectors reviewed the licensees corrective action program for trends that might be indicative of more significant safety issues:

(1) Procedural quality involving the adequacy of surveillance testing acceptance criteria and testing methodology
(2) Common cause analysis of the ANO Unit 1 Refueling Outage 1R27 human performance issues, Condition Report CR-ANO-C-2018-02728

Annual Follow-up of Selected Issues (1 Sample)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) Unit 2 failure of train A safety-related 4160 volt breaker 2A-303 to automatically close and service water pump B to start during surveillance testing on December 17, 2018

71153Follow-up of Events and Notices of Enforcement Discretion Events

(1) Unit 2 steam dump and bypass control system malfunction that caused an atmospheric dump valve to open and steam to enter the train A vital 4160 volt switchgear room on November 16, 2018
(2) Unit 1 automatic reactor trip due to the loss of the train A non-vital 4160 volt bus A1 on December 18, 2018

Licensee Event Reports (3 Samples)

The inspectors evaluated the following licensee event reports which can be accessed at https://lersearch.inl.gov/LERSearchCriteria.aspx:

(1) Licensee Event Report 0500313/2016-003-01, Tornado Vulnerabilities Resulting in Unanalyzed Condition Arkansas Nuclear One, Unit 1, on December 10, 2018
(2) Licensee Event Report 0500368/2017-001-00, Inadequate Protection from Tornado Missiles Identified Due to Nonconforming Design Conditions, on December 10, 2018
(3) Licensee Event Report 05000313/2018-002-01, Leak in Class 1 Reactor Coolant System Pressure Boundary Piping Due to Cyclic Fatigue Failure on a High Pressure Injection Line Drain Tap Weld, on November 16,

INSPECTION RESULTS

Failure to Fully Implement Vendor Manual Recommended Preventative Maintenance Cornerstone Significance Cross-cutting Aspect Inspection Procedure Mitigating Systems Green NCV 05000368/2018004-01 Closed None

71152 - Problem

Identification and Resolution The inspectors reviewed a self-revealed, Green finding and associated non-cited violation of Arkansas Nuclear One, Unit 2, Technical Specification 6.4.1.a, for the licensees failure to properly preplan maintenance that can affect the performance of safety-related equipment.

Specifically, the licensee failed to fully implement vendor manual recommended preventive maintenance for the shunt trip attachment switches. This resulted in the failure of train A safety-related breaker that provides power to the swing service water pump B (2P-4B) to automatically close and start pump 2P-4B during surveillance testing.

Description:

On October 23, 2018, the train A safety-related 4160 V switchgear 2A-303 breaker that provides power to pump 2P-4B failed to automatically close and start pump 2P-4B during surveillance testing. It was determined that an interlock on the train A safety-related 4160 V switchgear 2A-302 breaker that powers train A service water pump (2P-4A) prevented 2A-303 from automatically closing and starting pump 2P-4B. This interlock is designed to prevent both the 2P-4A and 2P-4B pumps from both automatically starting when aligned to emergency diesel generator 1. The interlock was comprised of a shunt trip attachment (STA) switch in the 2A-302 breaker. The licensee entered this issue into their corrective action program as Condition Report CR-ANO-2-2018-03454.

The licensee performed an equipment failure evaluation, documented in Condition Report CR-ANO-2-2018-03454, and determined that an oxide layer on the contacts of the STA switch for the 2A-302 breaker was the cause of the failure of 2A-303 to automatically close and start pump 2P-4B. A review of STA switch failures in the previous 10 years revealed that in 2009, a similar failure occurred and the corrective action was to incorporate vendor manual instructions to inspect and, if necessary, burnish (clean) the contacts when performing Procedure OP-2416.007, Unit 2 - 2A3 Bus Switchgear Inspection, Revision 17.

The licensee added this step into the work instructions to minimize oxide layer formation that would prevent the contacts on the STA switch from functioning. However, the updated work instructions did not fully incorporate the vendor manual recommended preventive maintenance. Specifically, the work instructions only gave instructions on how to clean the outer set of contacts and did not include direction on how to clean the harder to reach inner contacts. The licensee determined that the inner contacts were dirty and had caused the interlock to fail in this case.

The inspectors determined that this failure did not result in a technical specification violation because 2P-4B is a swing pump that could be powered from and connected to either train; during the period when it was assumed that it could not be started from the train A bus, the train A pump 2P-4A was in service and credited for technical specification compliance.

Corrective Actions: The licensee moved the interlock from the failed contact to a spare contact that they verified to be in good condition to restore operability of the pump. The licensee also performed an extent of condition evaluation to identify other failed safety-related and important to safety breakers. While several other contacts were in a condition that warranted cleaning, all of the other breakers tested would have functioned correctly if needed.

Corrective Action References: The licensee entered this issue into their corrective action program as Condition Reports CR-ANO-2-2018-03442, CR-ANO-2-2018-03454, and CR-ANO-2-2018-03750.

Performance Assessment:

Performance Deficiency: The licensees failure to fully implement vendor manual recommended preventive maintenance for STA contact switches is a performance deficiency.

Specifically, the licensee failed to provide maintenance instructions to clean the inner STA switch contacts that were in use, allowing them to become oxidized and develop a high resistance.

Screening: The inspectors determined the performance deficiency was more than minor, and therefore a finding, because it was associated with the equipment performance attribute of the Mitigating Systems Cornerstone and affected the associated cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (i.e., core damage). Specifically, the swing safety-related 4160 volt breaker 2A-303 was nonfunctional due to not fully implementing vendor recommended preventive maintenance on the inner half of the STA switches.

Significance: Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Exhibit 2, dated June 19, 2012, the inspectors determined that the finding had very low safety significance (Green) because the finding:

(1) was not a design or qualification deficiency;
(2) did not represent a loss of system and/or function;
(3) did not represent an actual loss of function of at least a single train for longer than its technical specification allowed outage time; and
(4) did not result in the loss of a high safety-significant, nontechnical specification train. Specifically, the 2P-4B pump was never credited for technical specification compliance during the period when it would not automatically start from the train A bus.

Cross-cutting Aspect: A cross-cutting aspect was not assigned to this finding because the performance deficiency occurred in 2009, and therefore was not indicative of current plant performance.

Enforcement:

Violation: Technical Specification 6.4.1.a for Unit 2 requires, in part, that written procedures be established, implemented, and maintained covering the applicable procedures listed in Appendix A to Regulatory Guide 1.33, Quality Assurance Program Requirements, Revision 2, dated February 1978. Regulatory Guide 1.33, Appendix A, Section 9.a, states, in part, that maintenance that can affect the performance of safety-related equipment should be properly preplanned and performed in accordance with written procedures, documented instructions, or drawings appropriate to the circumstances.

Contrary to the above, between October 2009 and October 2018, the licensee failed to properly pre-plan and perform maintenance that can affect performance of safety-related equipment in accordance with written procedures, document instructions, or drawings appropriate to the circumstances. Specifically, the licensee failed to maintain adequate work instructions to fully implement vendor recommended maintenance for safety-related breaker STA switch contacts when performing Procedure OP-2416.007, Unit 2 - 2A3 Bus Switchgear Inspection, Revision 17, Supplement 1, 2A3 Bus and Cubicle Inspection and Cleaning.

This condition led to the failure of the swing service water pump 2P-4B to automatically start during surveillance testing on October 23, 2018.

Disposition: This violation is being treated as a non-cited violation, consistent with Section 2.3.2 of the Enforcement Policy, because it was very low safety significance (Green)and was entered into the licensees corrective action program as Condition Reports CR-ANO-2-2018-03442, CR-ANO-2-2018-03454, and CR-ANO-2-2018-03750.

Observation

71152 - Problem

Identification and Resolution Semiannual Trend Review The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site.

The NRC inspectors identified a possible trend associated with the surveillance testing methodology and acceptance criteria. Examples included:

  • CR-ANO-1-2018-03223 and CR-ANO-2-2018-01009. The inspectors identified a minor violation of Unit 1 Technical Specification (TS) 5.4.1.a and Unit 2 TS 6.4.1.a for the licensees failure to maintain Unit 1 and Unit 2 Procedure OP-1102.001, Plant Pre-heat up and Pre-critical Checklist, Revision 83, and OP-2102.001, Plant Pre-heat up and Pre-critical Checklist, Revision 87, respectively. Specifically, the licensee did not actually measure seat leakage for some of the reactor coolant system (RCS)primary isolation valves (PIV) included in this surveillance test in accordance with American Society of Mechanical Engineers (ASME) Subsection ISTC-3630(c), Seat Leakage Measurement. The inspectors identified that the procedure inappropriately allowed recording a value of zero for the leak rate of several valves based on the measurements taken from the upstream check valve. The licensees corrective actions where to initiate procedure improvement forms to establish procedural steps to actually measure seat leakage in accordance with ASME Subsection ISTC-3630(c).
  • CR-ANO-1-2018-04304. The inspectors identified that Unit 1 Procedure OP-1104.036, Emergency Diesel Generator Operation, Revision 78, did not establish an acceptance criteria for check valve closure testing of diesel starting isolation check valves FO-54A1, FO-55A1, FO-54B1, and FO-55B1. Specifically, the licensee did not determine the maximum allowed check valve leakage to maintain diesel starting air system operability. The licensees corrective action was to determine the appropriate acceptance criteria to assure the valves are, in fact, closed. The licensee and the inspectors validated that the previous test results did not impact diesel starting air system operability.
  • CR-ANO-C-2018-04296. The inspectors identified a minor violation of Unit 1 TS 5.4.1.a and Unit 2 TS 6.4.1.a for the licensees failure to maintain Unit 1 and Unit 2 Procedure OP-1305.037, Unit 1 Reactor Building Access and Ventilation Leak Rate Testing, Revision 9, and OP-2305.017, Local Leak Rate Testing, Revision 36, respectively. Specifically, the licensee failed to translate Unit 1 TS 5.5.16 and Unit 2 TS 6.5.16 reactor building air lock operability limits as the acceptance criteria into procedures. The licensees corrective actions where to initiate PIFs to translate the TS operability limits as acceptance criteria into the respective procedure.
  • CR-ANO-2-2018-04357. The inspectors identified that Unit 2 Procedure OP-2106.006, Emergency Feedwater System Operations, Revision 98, testing methodology was not in accordance ASME code requirements and did not contain appropriate acceptance criteria for auxiliary feedwater to loop A/B emergency feedwater check valves 2EFW-28, 29, 30, and 31. Specifically, the acceptance criteria for the check valves was if downstream pressure was less than 10 psig or pressure was decreasing, record leakage as zero. The licensees corrective actions are:

1. Determine the design basis allowed leakage for valves 2EFW-28, 29, 30, and 31

and update the procedure and design basis documents.

2. Initiate a PIF to update the procedure to incorporate appropriate testing methods.

In response to the inspectors observations, the licensee entered this trend into their corrective action program for resolution as Condition Report CR-ANO-C-2019-00033.

Observation

71152 - Problem

Identification and Resolution Semiannual Trend Review

The inspectors reviewed the licensees corrective action program, performance indicators, system health reports, and other documentation available to help identify performance trends that might indicate the existence of a more significant safety issue. The inspectors verified that the licensee was taking corrective actions to address identified adverse trends. The inspectors did not review any cross-cutting themes because none existed at the site.

The inspectors reviewed the corrective action program documentation associated with the common cause analysis of the ANO Unit 1 Refueling Outage 1R27 performance issues, documented in Condition Report CR-ANO-C-2018-02728. The inspectors identified 12 documented human performance errors that caused events, rework, and delays. The licensee initiated the condition report following these events in an effort to document and discover how to prevent these issues from continuing to occur. The licensee identified five causal factors and developed a corrective action for each:

1. Insufficient ownership and accountability by licensee and supplemental personnel

resulted in a tolerance of low standards in sustaining nuclear professional behaviors by individual contributors and leadership. Corrective Action (CA) included:

  • Integrate the Own It Accountability Model in work preparation/execution activities into the licensees work preparation meetings to improve ownership and accountability in the pursuit of excellence for licensee work preparation and execution.
  • Implement a licensee Organization Effectiveness Top Issues List and use the organization effectiveness model, administrative tools, and communications media forums to keep issues visible and track to resolution.
  • Pursuit of Craftsmanship Excellence Committee. The pursuit of craftsmanship excellence through the engagement and ownership of supplemental personnel focused on improving craftsmanship, work quality, maintenance technical fundamentals, and sustaining nuclear professional behaviors.
  • Senior leadership team to partner with the first line supervisors leadership council to promote greater ownership, engagement and accountability to address licensee top first-line supervisory issues.
  • Conduct a Unit 2 Refueling Outage 2R26 pre-outage leadership and alignment meeting with licensee and supplemental leaders to reset the standards and expectations for 2R26 work preparation and execution.

2. Management and peer coaching did not consistently correct unacceptable behaviors

due to the tendency of some leaders to avoid conflict and difficult conversions.

Corrective actions included:

  • Manager leadership by example and field presence. The intent of this action was to drive and set an example for management oversight of the preparation and execution of outage maintenance critical activities.
  • Reinforce the expectations for detailed pre-job briefs and perform observations focused on pre-job briefs to validate standards are met. The intent of this action was to verify monthly that licensee and supplemental leader observation quality was documented in accordance with the observation excellence model and to provide coaching to correct identified gaps.
  • Incorporate observation goals into the 2018 personnel performance reviews.

The intent of this action was to ensure leaders are driving the right behavior changes in the organization.

  • Commence rapid trending of observation data.

3. Licensee personal became complacent to the requirements for strict adherence to

procedures and work instructions due to the lack of immediate consequence for noncompliance. Corrective actions included:

  • Implement remediation model for procedure/work instruction adherence. The intent of this action was to provide clear management expectations and accountability at all levels of the organization for procedure and work instruction adherence.
  • Incorporate Procedure EN-HU-106, Procedure and Work Instructions Use and Adherence, Revision 7, training into maintenance continuing training.

4. Risk was not always recognized or was inappropriately accepted by individuals without

sufficient leadership engagement in real time decision-making. Corrective actions included:

==2R26 standards team focus on real-time decision-making (stop when unsure).

==

The intent of this action was to ensure the 2R26 standards team plan included a focus area for field observations related to stop when unsure (real-time decision making) and pre-job briefs (work preparation, roles and responsibilities, and risk mitigation).

2R26 personnel briefing on unknowingly accepting station risk. The intent of

this action was to provide communication to 2R26 works to increase the awareness of unknowingly making decisions in the field that may increase station risk.

5. Licensee leadership did not consistently manage and control outage work scope which

impacted the stations ability to effectively prepare and execute scheduled work activities. Corrective actions included:

  • Validate effective change management when 2R26 major work was reassigned near the outage. The intent of this action was to provide effective change management for scoping transitions that occur within 60 days of schedule start date for 2R26.
  • Establish unit specific outage work scope priority lists. The intent of this action was clearly defined outage work scope priorities and to control the combined outage work scope within budgeted resources and margins to allow adequate time for work preparation and execution using the prevention model.
  • Perform an independent verification that major projects are ready for execution prior to 2R26. The intent of this action was clearly defined outage work scope priorities and control the combined outage work scope within budgeted resources and margins to allow adequate time for work preparation and execution using the prevention model.

The inspectors observed actions implemented during ANO Unit 2 Refueling Outage 2R26 and noted that the number of events, rework, and delays decreased dramatically during Refueling Outage 2R26 as a result. Although several performance issues still occurred, the inspectors determined that the ongoing actions to minimize these issues are being implemented successfully. For this trend, the inspectors determined that the licensee had identified the trend, completed an appropriate evaluation, and had taken actions to correct the identified trend.

EXIT MEETINGS AND DEBRIEFS

On December 14, 2018, the inspector presented the emergency action level revision review inspection results to Mr. A. Sherrill, Manager, Emergency Preparedness, and other members of the licensee staff. The inspectors verified no proprietary information was retained or documented in this report.

On January 3, 2019, the inspector presented the quarterly resident inspector inspection results to Mr. J. Kirkpatrick, General Manager of Plant Operations, and other members of the licensee staff. The inspectors verified no proprietary information was retained or documented in this report.

DOCUMENTS REVIEWED

71111.04 - Equipment Alignment

Condition Reports (CR-ANO-)

1-2012-00362

1-2012-00363

1-2018-04976

C-2016-01706

Procedures

Number

Title

Revision

OP-1104.002

Makeup and Purification System Operation

OP-1106.006

Emergency Feedwater Operations

101

OP-1107.001

Electrical System Operations

20

OP-2106.006

Emergency Feedwater Operations

Miscellaneous

Documents

Number

Title

Revision

EC-65360

CALC-82-D-2086-01 Mark Up to Account for

Condensate Lost due to Pump Bearing and Correct

Computation Error

Calculations

Number

Title

Revision

CALC-82-D-2086-

Volume of CST T-41B Requiring Tornado Missile

Protection

71111.05 - Fire Protection

Condition Reports (CR-ANO-)

2-2018-04226

Miscellaneous

Documents

Number

Title

1A-372-86-G

Unit 1 Plant Fire Protection

1B-317-10-EE

Unit 1 Plant Fire Protection

1B-335-38-Y

Unit 1 Plant Fire Protection

2A-404-2151-A

Unit 2 Plant Fire Protection

71111.07 - Heat Sink Performance

Work Orders

503112

2675121

2769910

2770785

2770786

Procedures

Number

Title

Revision

OP-2305.062

Service Water System Flow Testing

Miscellaneous

Documents

Number

Title

Revision

EC-72776

Document the Results of the 2R25 As-Left Service

Water Flow Test

Calculations

Number

Title

Revision

CALC-88-E-0032-

Unit 2 Containment Service Water Cooling Coils Thermal

Performance

CALC-91-R-2013-

Service Water Performance Testing Methodology

CALC-99-E-0033-

ANO-2 Containment Cooler Fan Motor Horsepower

during a DBA Under Uprate Conditions

CALC-

991522E201-01

Determination of Error Associated with Air Flow

Measurements of Reactor Building Containment Coolers

71111.11 - Licensed Operator Requalification Program

Miscellaneous

Documents

Number

Title

Revision

A1SXMLOR1902

Unit 1 Licensed Operation Requalification Scenario

71111.12 -Maintenance Effectiveness

Condition Reports (CR-ANO-)

C-2018-03631

Work Orders

00486027

Procedures

Number

Title

Revision

EN-DC-207

Maintenance Rule Periodic Assessment

Drawings

Number

Title

E-2258

Schematic Diagram Reactor Control Element Assembly

M-2001-L1-196

CEDMCS Schematic Diagram Subgroup Filter Panel

Calculations

Number

Title

Revision

CALC-ANOC-SE-

17-00001

Maintenance Rule 10 CFR 50.65(a)(3) Periodic

Assessment January 1, 2016, to June 30, 2017

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Condition Reports (CR-ANO-)

2-2018-02847

2-2018-02909

Procedures

Number

Title

Revision

2102.010

Plant Cooldown

Miscellaneous

Documents

Number

Title

Revision

NUREG 1022

Event Report Guidelines 10 CFR 50.72 and 50.73

71111.15 - Operability Determinations and Functionality Assessments

Condition Reports (CR-ANO-)

1-2015-02718

1-2018-04619

1-2018-04636

1-2018-04668

1-2018-04671

1-2018-04674

2-2013-01190

2-2018-02976

2-2018-03127

2-2018-03252

2-2018-03304

Procedures

Number

Title

Revision

EN-OP-104

Operability Determination Process

Miscellaneous

Documents

Number

Title

Date

EC-79912

Engineering Change

EC-80182

Engineering Change

EC-79906

Engineering Change

N-705

Evaluation Criteria for Temporary Acceptance of

Degradation in Moderate Energy Class 2 or 3 Vessels

and Tanks

October 12,

2006

Calculations

Number

Title

Revision

CALC-ANO2-ME-

18-00003

Evaluation of Safety Injection Nozzles and Thermal

Sleeves Supporting Justification for Continued Operation

at ANO2

Calculations

Number

Title

Revision

CALC-ANO2-ME-

18-00004

Operability Assessment for Primary Side Loose Parts

from Migration of Safety Injection Nozzle Thermal Sleeve

at Arkansas Nuclear One Unit 2

71111.18 - Plant Modifications

Condition Reports (CR-ANO-)

2-2018-04166

Work Orders

471461

2940

2790774

Procedures

Number

Title

Revision

OP-2302.046

CEA Drop Time Test

ULD-2-SYS-36

Control Element Drive Mechanism

Miscellaneous

Documents

Number

Title

Revision

EC-75702

Replace CEA Upper Gripper Coils with Westinghouse

High Temp Coils

EC-78985

Amend Low Voltage Setting for HT Upper Gripper Coils

EC-80516

ANO-2 CEA Drop Time Uncertainty Relaxation

71111.19 - Post Maintenance Testing

Condition Reports (CR-ANO-)

1-2018-05315

1-2018-05328

1-2018-05350

2-2018-02213

2-2018-03919

2-2018-04002

2-2018-04166

2-2018-04446

Work Orders

2399

486741

509778

2499

2940

2573102

2776588

2790774

2805699

Procedures

Number

Title

Revision

OP-2102.001

Plant Pre-heatup and Pre-critical Checklist

OP-2302.046

CEA Drop Time Test

OP-2305.001

Integrated Engineering Safeguards Test

OP-2305.017

Local Leak Rate Testing

71111.20 - Refueling and Other Outage Activities

Condition Reports (CR-ANO-)

1-2018-05325

2-2018-02129

2-2018-02130

C-2018-04030

Work Orders

2770782

Procedure

Number

Title

Revision

OP-2306.024

Unit 2 (IST) Relief Valve Setpoint Testing

OP-2505.004

Unit 2 Core Support Barrel Removal

71111.22 - Surveillance Testing

Condition Reports (CR-ANO-)

1-2018-00963

1-2018-04790

1-2018-04795

1-2018-04975

2-2004-01688

2-2018-04357

C-2018-04296

C-2018-04339

Work Orders

486741

2573102

2719205

2764513

2770817

2771820

2780270

2815431

Procedures

Number

Title

Revision

ER-ANO-2006-

0389-000

U2 EFW Alignment to QCST Evaluation

OP-1305.037

Unit 1 Reactor Building Access and Ventilation Leak

Rate Testing

(8)

OP-2106.006

Emergency Feedwater System Operation

OP-2305.001

Integrated Engineering Safeguards Test

OP-2305.017

Local Leak Rate Testing

SEP-ANO-2-IST-1 Inservice Testing Bases Document

SEP-APJ-002

Arkansas Nuclear One Containment Leakage Rate

Testing (Appendix J)

ULD-2-SYS-12

Emergency Feedwater System

Miscellaneous

Documents

Number

Title

Revision

M-2204, Sheet

P&ID

Emergency Feedwater

Calculations

Number

Title

Revision

CALC-00-E-0010-

Appendix J Containment Maximum Allowable Leakage

Rate (La)

CALC-00-E-0023-

Unit 1 Appendix J Containment Maximum Allowable

Leakage Rate (La)

CALC-89-D-2043-

Failure Modes Effect Analysis for the Addition of the

Auxiliary Feedwater Pump

71114.04 - Emergency Action Level and Emergency Plan Changes

Procedures

Number

Title

Revision

1903.010

Emergency Action Level Classification

44, 56

Miscellaneous

Documents

Number

Title

Date

0CAN101801

Emergency Plan Implementing Procedure, Arkansas

Nuclear One, Units 1 and 2,

Docket Nos. 50-313, 50-368, and 72-13; License

Nos. DPR-51 and NPF-6

October 4, 2018

71151 - Performance Indicator Verification

Condition Reports (CR-ANO-)

1-2017-03024

1-2018-03729

Procedures

Number

Title

Revision

EN-LI-114

Regulatory Performance Indicator Process

Calculations

Number

Title

Revision

CALC-ANO1-SA-

16-00001

ANO-1 Mitigating System Performance Index Basis

CALC-ANO2-SA-

06-00001

ANO-2 Mitigating System Performance Index Basis

71152 - Problem Identification and Resolution

Condition Reports (CR-ANO-)

1-2018-00963

1-2018-04296

1-2018-04790

1-2018-04975

C-2018-04339

2-2018-03442

2-2018-03442

2-2018-03454

2-2018-03750

2-2009-02997

1-2018-03223

2-2018-01009

1-2018-04304

C-2018-04296

2-2018-04357

C-2019-00033

Work Orders

411600

511409

2775094

Procedures

Number

Title

Revision

OP-1305.037

Unit 1 Reactor Building Access and Ventilation Leak

Rate Testing

(8)

OP-2416.007

Unit 2 - 2A3 Bus Switchgear Inspection

Miscellaneous

Documents

Number

Title

PIF 1-18-0125

Procedure Improvement Form for OP-1305.037

71153 - Follow-up of Events and Notices of Enforcement Discretion

Condition Reports (CR-ANO-)

1-2017-00241

1-2018-05311

1-2018-05312

1-2018-05326

1-2018-05332

1-2018-05340

1-2018-05360

2-2017-01555

2-2018-04225

2-2018-04226

2-2018-04227

2-2018-04230

2-2018-04241

2-2018-04244

2-2018-04336

C-2018-04699

Procedures

Number

Title

Revision

203.012B

Annunciator 2K02 Corrective Action

EN-OP-126

Post Transient Response and Review

Drawings

Number

Title

Revision

2HBD-300-1

Small Pipe Isometric Auxiliary Building

2HBD-300-2

Small Pipe Isometric Turbine Building

A-2103

Architectural Floor Plan at el 368, 372, and 374 6

A-2104

Architectural Floor Plan at el 386

A-2114

Architectural Exterior Elevations and Sections

E-34

Schematic Meter and Relay Diagram 4160V System,

Main Supply

M-2112

Plumbing and Drainage Aux Bldg

M-2116

Plumbing and Drainage Aux Bldg

Miscellaneous

Documents

Number

Title

Revision

STM 2-15

Steam Generators and Main Steam System

STM 2-23

Steam Dump and Bypass Control System

ML19024A075

SUNSI Review

ADAMS:

Non-Publicly Available

Non-Sensitive

Keyword:

By: NOKeefe

Yes No

Publicly Available

Sensitive

NRC-002

OFFICE

SRI:DRP/D

RI:DRP/D

RI:DRP/D

BC:DRS/EB1

ABC:DRS/EB2

BC:DRS/OB

NAME

CHenderson

MTobin

TSullivan

VGaddy

JDrake

GWerner

SIGNATURE

cmh

MCT

TMS

vgg

JFD

GEW

DATE

1/10/2019

1/10/2019

1/10/2019

1/14/19

1/14/19

01/12/2019

OFFICE

BC:DRS/PSB2

ATL:DRS/IPAT

BC:DRP/D

NAME

HGepford

RKellar

NOKeefe

SIGNATURE

hjg

RLK

NFO

DATE

01/14/2019

01/14/2019

1/23/19