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{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION REGION II SAM NUNN ATLANTA FEDERAL CENTER 61 FORSYTH STREET, SW, SUITE 23T85 ATLANTA, GEORGIA 30303-8931 February 5, 2010 Mr. Michael Vice President Carolina Power and Light Company Brunswick Steam Electric Plant P. O. Box 10429 Southport, NC 28461
{{#Wiki_filter:UNITED STATES NUCLEAR REGULATORY COMMISSION ruary 5, 2010


SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA
==SUBJECT:==
BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA


==Dear Mr. Annacone:==
==Dear Mr. Annacone:==
Line 31: Line 32:


Sincerely,
Sincerely,
/RA/ Randall A. Musser, Chief Reactor Projects Branch 4 Division of Reactor Projects  
/RA/
Randall A. Musser, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket No.: 50-325, 50-324 License No.: DPR-71, DPR-62 Enclosure: Inspection Report 05000325, 324/2009003 cc w\encls: See page 2


Docket No.: 50-325, 50-324 License No.: DPR-71, DPR-62 Enclosure: Inspection Report 05000325, 324/2009003 cc w\encls: See page 2
_________________________  XG SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRP SIGNATURE GJW /RA/ JGW /RA/ RAM /RA/
NAME  GWilson JWorosilo RMusser DATE  02/05/2010 02/05/2010 02/05/2010 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO


_________________________ X G SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRP SIGNATURE GJW /RA/ JGW /RA/ RAM /RA/ NAME GWilson JWorosilo RMusser DATE 02/05/2010 02/05/2010 02/05/2010 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO CP&L 2 cc w/encl: R. J. Duncan, II Vice President Nuclear Operations Carolina Power & Light Company Electronic Mail Distribution Director Site Operations Brunswick Steam Electric Plant Electronic Mail Distribution Edward L. Wills, Jr. Plant General Manager Brunswick Steam Electric Plant Progress Energy Carolinas, Inc. Electronic Mail Distribution
CP&L   2 cc w/encl:   Annette H. Pope R. J. Duncan, II Supervisor, Licensing/Regulatory Programs Vice President Brunswick Steam Electric Plant Nuclear Operations  Progress Energy Carolinas, Inc.


Christos Kamilaris, Director Fleet Support Services Carolina Power & Light Company Electronic Mail Distribution  
Carolina Power & Light Company Electronic Mail Distribution Electronic Mail Distribution Senior Resident Inspector Director Site Operations  U.S. Nuclear Regulatory Commission Brunswick Steam Electric Plant Brunswick Steam Electric Plant Electronic Mail Distribution U.S. NRC 8470 River Road, SE Edward L. Wills, Jr. Southport, NC 28461 Plant General Manager Brunswick Steam Electric Plant John H. O'Neill, Jr.


Joseph W. Donahue, Vice President Nuclear Oversight Carolina Power and Light Company Electronic Mail Distribution  
Progress Energy Carolinas, Inc. Shaw, Pittman, Potts & Trowbridge Electronic Mail Distribution 2300 N. Street, NW Washington, DC 20037-1128 Christos Kamilaris, Director Fleet Support Services  Peggy Force, Assistant Attorney General Carolina Power & Light Company State of North Carolina Electronic Mail Distribution P.O. Box 629 Raleigh, NC 27602 Joseph W. Donahue, Vice President Nuclear Oversight Chairman, Carolina Power and Light Company North Carolina Utilities Commission Electronic Mail Distribution Electronic Mail Distribution Brian C. McCabe  Robert P. Gruber, Executive Director Manager, Nuclear Regulatory Affairs Public Staff - NCUC Progress Energy Carolinas, Inc. 4326 Mail Service Center Electronic Mail Distribution Raleigh, NC 27699-4326 Phyllis N. Mentel  Brunswick County Board of Commissioners Manager, Support Services  P.O. Box 249 Brunswick Steam Electric Plant Bolivia, NC 28422 Progress Energy Carolinas, Inc.


Brian C. McCabe Manager, Nuclear Regulatory Affairs Progress Energy Carolinas, Inc. Electronic Mail Distribution  
Electronic Mail Distribution James Ross, Nuclear Energy Institute Electronic Mail Distribution Michael S. Williams, Manager, Training Brunswick Steam Electric Plant Public Service Commission Progress Energy Carolinas, Inc. State of South Carolina Electronic Mail Distribution P.O. Box 11649 Columbia, SC 29211 (Vacant)
Manager  cc w/encl. (continued next page)
License Renewal Progress Energy Electronic Mail Distribution


Phyllis N. Mentel Manager, Support Services Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.
CP&L  3 cc w/encl. (continued)
W. Lee Cox, II, Section Chief Radiation Protection Section N.C. Department of Environmental Commerce & Natural Resources Electronic Mail Distribution Warren Lee Emergency Management Director New Hanover County Department of Emergency Management 230 Government Center Drive Suite 115 Wilmington, NC 28403


Electronic Mail Distribution Michael S. Williams, Manager, Training Brunswick Steam Electric Plant Progress Energy Carolinas, Inc. Electronic Mail Distribution
CP&L  4 Letter to Michael from Randall A. Musser dated February 5, 2010 SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA Distribution w/encl:
C. Evans, RII EICS L. Slack, RII EICS OE Mail RIDSNRRDIRS PUBLIC R. Pascarelli, NRR ((Regulatory Conferences Only))
RidsNrrPMBrunswick Resource


(Vacant) Manager License Renewal Progress Energy Electronic Mail Distribution
with the PI data collected or transmitted for this indicator and none were identified.


Annette H. Pope Supervisor, Licensing/Regulatory Programs Brunswick Steam Electric Plant Progress Energy Carolinas, Inc.
Specific documents reviewed are described in the Appendix to this report.


Electronic Mail Distribution Senior Resident Inspector U.S. Nuclear Regulatory Commission Brunswick Steam Electric Plant U.S. NRC 8470 River Road, SE Southport, NC 28461 John H. O'Neill, Jr. Shaw, Pittman, Potts & Trowbridge 2300 N. Street, NW Washington, DC 20037-1128 Peggy Force, Assistant Attorney General State of North Carolina P.O. Box 629 Raleigh, NC 27602 Chairman, North Carolina Utilities Commission Electronic Mail Distribution
* Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report.


Robert P. Gruber, Executive Director Public Staff - NCUC 4326 Mail Service Center Raleigh, NC 27699-4326
b. Findings No findings of significance were identified.


Brunswick County Board of Commissioners P.O. Box 249 Bolivia, NC 28422
4OA2 Identification and Resolution of Problems
.1 Routine Review of Items Entered Into the Corrective Action Program a. Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensees corrective action program. The review was accomplished by reviewing daily action request reports.


James Ross, Nuclear Energy Institute Electronic Mail Distribution Public Service Commission State of South Carolina P.O. Box 11649 Columbia, SC 29211
b. Findings No findings of significance were identified.


cc w/encl. (continued next page)
.2 Semi-Annual Trend Review a. Scope The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted.
CP&L 3 cc w/encl. (continued) W. Lee Cox, II, Section Chief Radiation Protection Section N.C. Department of Environmental Commerce & Natural Resources Electronic Mail Distribution Warren Lee Emergency Management Director New Hanover County Department of Emergency Management 230 Government Center Drive Suite 115 Wilmington, NC 28403 CP&L 4 Letter to Michael from Randall A. Musser dated February 5, 2010 SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA Distribution w/encl:
C. Evans, RII EICS L. Slack, RII EICS OE Mail RIDSNRRDIRS PUBLIC R. Pascarelli, NRR ((Regulatory Conferences Only)) RidsNrrPMBrunswick Resource 19 Enclosure with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Appendix to this report.


* Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensee's operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report. b. Findings No findings of significance were identified. 4OA2 Identification and Resolution of Problems
Enclosure
.1 Routine Review of Items Entered Into the Corrective Action Program a. Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensee's corrective action program. The review was accomplished by reviewing daily action request reports. b. Findings No findings of significance were identified. .2 Semi-Annual Trend Review a. Scope The inspectors performed a review of the licensee's CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors' review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors'
review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted.


20 Enclosure The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensee's CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensee's trending reports were reviewed for adequacy. b. Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:
The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.
* Improper loosening of RPV reference leg connection, NCR# 322354
* Unit 2 interruption of Shutdown Cooling due to maintenance, NCR# 327475
* Rx Hydro core spray check valve high pressure test jumper failure, NCR# 329677
* Work accomplished with inadequate documentation, NCR# 330266
* Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004 The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.


.3 Selected Issue Follow-up Inspection: 1B Fuel Pool Filter Leak
b. Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:
* Improper loosening of RPV reference leg connection, NCR# 322354
* Unit 2 interruption of Shutdown Cooling due to maintenance, NCR# 327475
* Rx Hydro core spray check valve high pressure test jumper failure, NCR# 329677
* Work accomplished with inadequate documentation, NCR# 330266
* Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004 The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.


a. Inspection Scope The inspectors selected AR #335654, 1B Fuel Pool Filter Leak for detailed review. This AR was associated with a an entry into AOP 5.0, Radioactive Spills, High Radiation, and Airborne Radioactivity, due to a leak from the 1B fuel pool filter gasket. The inspectors reviewed this report to verify that the licensee identified the full extent of the issue, performed an appropriate evaluation, and specified and prioritized appropriate corrective actions. The inspectors evaluated the report against the requirements of the licensee's corrective action program as delineated in corporate procedure CAP-NGGC-0200, Corrective Action Program, and 10 CFR 50, Appendix B.
.3 Selected Issue Follow-up Inspection: 1B Fuel Pool Filter Leak a. Inspection Scope The inspectors selected AR #335654, 1B Fuel Pool Filter Leak for detailed review. This AR was associated with a an entry into AOP 5.0, Radioactive Spills, High Radiation, and Airborne Radioactivity, due to a leak from the 1B fuel pool filter gasket. The inspectors reviewed this report to verify that the licensee identified the full extent of the issue, performed an appropriate evaluation, and specified and prioritized appropriate corrective actions. The inspectors evaluated the report against the requirements of the licensees corrective action program as delineated in corporate procedure CAP-NGGC-0200, Corrective Action Program, and 10 CFR 50, Appendix B.


b. Findings No findings of significance were identified.
b. Findings No findings of significance were identified.


4OA5 Other Activities
4OA5 Other Activities
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities a. Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee 21 Enclosure security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities. b. Findings No findings of significance were identified. 4OA6 Management Meetings
.1 Quarterly Resident Inspector Observations of Security Personnel and Activities a. Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee Enclosure
.1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period. An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.
 
security procedures and regulatory requirements relating to nuclear plant security.


ATTACHMENT: SUPPLEMENTAL INFORMATION 19 Enclosure with the PI data collected or transmitted for this indicator and none were identified. Specific documents reviewed are described in the Appendix to this report. Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensee's operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report. a. Findings No findings of significance were identified. 4OA2 Identification and Resolution of Problems
These observations took place during both normal and off-normal plant working hours.
.1 Routine Review of Items Entered Into the Corrective Action Program a. Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensee's corrective action program. The review was accomplished by reviewing daily action request reports. b. Findings No findings of significance were identified. .2 Semi-Annual Trend Review a. Scope The inspectors performed a review of the licensee's CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors' review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors' review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted. The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance 20 Enclosure reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensee's CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensee's trending reports were reviewed for adequacy. b. Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:


Improper loosening of RPV reference leg connection, NCR# 322354 Unit 2 interruption of Shutdown Cooling due to maintenance, NCR# 327475 Rx Hydro core spray check valve high pressure test jumper failure, NCR#
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.
329677 Work accomplished with inadequate documentation, NCR# 330266 Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004 The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.
 
b. Findings No findings of significance were identified.
 
4OA6 Management Meetings
.1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.
 
An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.
 
ATTACHMENT: SUPPLEMENTAL INFORMATION Enclosure
 
with the PI data collected or transmitted for this indicator and none were identified.
 
Specific documents reviewed are described in the Appendix to this report.
 
y Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report.
 
a. Findings No findings of significance were identified.
 
4OA2 Identification and Resolution of Problems
.1 Routine Review of Items Entered Into the Corrective Action Program a. Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensees corrective action program. The review was accomplished by reviewing daily action request reports.
 
b. Findings No findings of significance were identified.
 
.2 Semi-Annual Trend Review a. Scope The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted.
 
The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance Enclosure
 
reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.
 
b. Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:
y Improper loosening of RPV reference leg connection, NCR# 322354 y Unit 2 interruption of Shutdown Cooling due to maintenance, NCR# 327475 y Rx Hydro core spray check valve high pressure test jumper failure, NCR#
329677 y Work accomplished with inadequate documentation, NCR# 330266 y Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004 The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.


4OA5 Other Activities
4OA5 Other Activities
  .1 Quarterly Resident Inspector Observations of Security Personnel and Activities a. Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security. These observations took place during both normal and off-normal plant working hours. These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities. b. Findings No findings of significance were identified. 4OA6 Management Meetings
  .1 Quarterly Resident Inspector Observations of Security Personnel and Activities a. Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.
 
These observations took place during both normal and off-normal plant working hours.
 
These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.
 
b. Findings No findings of significance were identified.
 
4OA6 Management Meetings
  .1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.
  .1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.


21 Enclosure An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.
Enclosure
 
An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.


ATTACHMENT: SUPPLEMENTAL INFORMATION
ATTACHMENT: SUPPLEMENTAL INFORMATION Enclosure
}}
}}

Revision as of 22:02, 13 November 2019

IR 05000325-09-003 & 05000324-09-003, on 07/30/09, Brunswick Steam Electric Plant
ML100360622
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 02/05/2010
From: Randy Musser
NRC/RGN-II/DRP/RPB4
To: Annacone M
Carolina Power & Light Co
References
ML092110250 IR-09-003
Download: ML100360622 (21)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION ruary 5, 2010

SUBJECT:

BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA

Dear Mr. Annacone:

On July 30, 2009, the US Nuclear Regulatory Commission (NRC) issued the subject inspection report for the Brunswick Steam Electric Plant, ADAMS accession ML092110250. In reviewing this report, it was noted that we inadvertently omitted the Selected Issue Follow-up Inspection in section 4OA2.3. Accordingly, we are providing a revised version of Inspection Report 05000325/324/2009003 that documents the above change.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (The Public Electronic Reading Room).

I apologize for any inconvenience this error may have caused. If you have any questions, please contact me at (404) 562-4603.

Sincerely,

/RA/

Randall A. Musser, Chief Reactor Projects Branch 4 Division of Reactor Projects Docket No.: 50-325, 50-324 License No.: DPR-71, DPR-62 Enclosure: Inspection Report 05000325, 324/2009003 cc w\encls: See page 2

_________________________ XG SUNSI REVIEW COMPLETE OFFICE RII:DRP RII:DRP RII:DRP SIGNATURE GJW /RA/ JGW /RA/ RAM /RA/

NAME GWilson JWorosilo RMusser DATE 02/05/2010 02/05/2010 02/05/2010 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

CP&L 2 cc w/encl: Annette H. Pope R. J. Duncan, II Supervisor, Licensing/Regulatory Programs Vice President Brunswick Steam Electric Plant Nuclear Operations Progress Energy Carolinas, Inc.

Carolina Power & Light Company Electronic Mail Distribution Electronic Mail Distribution Senior Resident Inspector Director Site Operations U.S. Nuclear Regulatory Commission Brunswick Steam Electric Plant Brunswick Steam Electric Plant Electronic Mail Distribution U.S. NRC 8470 River Road, SE Edward L. Wills, Jr. Southport, NC 28461 Plant General Manager Brunswick Steam Electric Plant John H. O'Neill, Jr.

Progress Energy Carolinas, Inc. Shaw, Pittman, Potts & Trowbridge Electronic Mail Distribution 2300 N. Street, NW Washington, DC 20037-1128 Christos Kamilaris, Director Fleet Support Services Peggy Force, Assistant Attorney General Carolina Power & Light Company State of North Carolina Electronic Mail Distribution P.O. Box 629 Raleigh, NC 27602 Joseph W. Donahue, Vice President Nuclear Oversight Chairman, Carolina Power and Light Company North Carolina Utilities Commission Electronic Mail Distribution Electronic Mail Distribution Brian C. McCabe Robert P. Gruber, Executive Director Manager, Nuclear Regulatory Affairs Public Staff - NCUC Progress Energy Carolinas, Inc. 4326 Mail Service Center Electronic Mail Distribution Raleigh, NC 27699-4326 Phyllis N. Mentel Brunswick County Board of Commissioners Manager, Support Services P.O. Box 249 Brunswick Steam Electric Plant Bolivia, NC 28422 Progress Energy Carolinas, Inc.

Electronic Mail Distribution James Ross, Nuclear Energy Institute Electronic Mail Distribution Michael S. Williams, Manager, Training Brunswick Steam Electric Plant Public Service Commission Progress Energy Carolinas, Inc. State of South Carolina Electronic Mail Distribution P.O. Box 11649 Columbia, SC 29211 (Vacant)

Manager cc w/encl. (continued next page)

License Renewal Progress Energy Electronic Mail Distribution

CP&L 3 cc w/encl. (continued)

W. Lee Cox, II, Section Chief Radiation Protection Section N.C. Department of Environmental Commerce & Natural Resources Electronic Mail Distribution Warren Lee Emergency Management Director New Hanover County Department of Emergency Management 230 Government Center Drive Suite 115 Wilmington, NC 28403

CP&L 4 Letter to Michael from Randall A. Musser dated February 5, 2010 SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION REPORT NOS.: 05000325/2009003, 05000324/2009003 ERRATA Distribution w/encl:

C. Evans, RII EICS L. Slack, RII EICS OE Mail RIDSNRRDIRS PUBLIC R. Pascarelli, NRR ((Regulatory Conferences Only))

RidsNrrPMBrunswick Resource

with the PI data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the Appendix to this report.

  • Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report.

b. Findings No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Items Entered Into the Corrective Action Program a. Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensees corrective action program. The review was accomplished by reviewing daily action request reports.

b. Findings No findings of significance were identified.

.2 Semi-Annual Trend Review a. Scope The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted.

Enclosure

The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.

b. Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:

  • Improper loosening of RPV reference leg connection, NCR# 322354
  • Work accomplished with inadequate documentation, NCR# 330266
  • Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004 The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.

.3 Selected Issue Follow-up Inspection: 1B Fuel Pool Filter Leak a. Inspection Scope The inspectors selected AR #335654, 1B Fuel Pool Filter Leak for detailed review. This AR was associated with a an entry into AOP 5.0, Radioactive Spills, High Radiation, and Airborne Radioactivity, due to a leak from the 1B fuel pool filter gasket. The inspectors reviewed this report to verify that the licensee identified the full extent of the issue, performed an appropriate evaluation, and specified and prioritized appropriate corrective actions. The inspectors evaluated the report against the requirements of the licensees corrective action program as delineated in corporate procedure CAP-NGGC-0200, Corrective Action Program, and 10 CFR 50, Appendix B.

b. Findings No findings of significance were identified.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities a. Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee Enclosure

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.

b. Findings No findings of significance were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.

An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.

ATTACHMENT: SUPPLEMENTAL INFORMATION Enclosure

with the PI data collected or transmitted for this indicator and none were identified.

Specific documents reviewed are described in the Appendix to this report.

y Safety System Functional Failures The inspectors reviewed licensee submittals for the Safety System Functional Failures performance indicator for the period from the second quarter of 2008 through the first quarter of 2009. The inspectors reviewed the licensees operator narrative logs, operability assessments, maintenance rule records, maintenance work orders, issue reports, event reports and NRC Integrated Inspection reports for the period to validate the accuracy of the submittals. Specific documents reviewed are described in the Appendix to this report.

a. Findings No findings of significance were identified.

4OA2 Identification and Resolution of Problems

.1 Routine Review of Items Entered Into the Corrective Action Program a. Scope To aid in the identification of repetitive equipment failures or specific human performance issues for follow-up, the inspectors performed frequent screenings of items entered into the licensees corrective action program. The review was accomplished by reviewing daily action request reports.

b. Findings No findings of significance were identified.

.2 Semi-Annual Trend Review a. Scope The inspectors performed a review of the licensees CAP and associated documents to identify trends that could indicate the existence of a more significant safety issue. The inspectors review was focused on repetitive equipment issues, but also considered the results of daily inspector CAP item screening discussed in Section 4OA2.1 above, licensee trending efforts, and licensee human performance results. The inspectors review nominally considered the six-month period of January 2009 through June 2009, although some examples expanded beyond those dates where the scope of the trend warranted.

The review also included issues documented outside the normal CAP in major equipment problem lists, repetitive and/or rework maintenance lists, departmental problem/challenges lists, system health reports, quality assurance audit/surveillance Enclosure

reports, self assessment reports, and Maintenance Rule assessments. The inspectors compared and contrasted their results with the results contained in the licensees CAP trending reports. Corrective actions associated with a sample of the issues identified in the licensees trending reports were reviewed for adequacy.

b. Assessment and Observations No findings of significance were identified. The inspectors noted a trend in procedure adherence and the work management process. In particular, adverse effects had been identified on system performance. This was exemplified by the following identified issues:

y Improper loosening of RPV reference leg connection, NCR# 322354 y Unit 2 interruption of Shutdown Cooling due to maintenance, NCR# 327475 y Rx Hydro core spray check valve high pressure test jumper failure, NCR#

329677 y Work accomplished with inadequate documentation, NCR# 330266 y Improperly performed procedure step during 0MST-PCIS41R, NCR# 331004 The inspectors concluded that while the licensee has been providing additional focus and training to this area, more attention and follow-up is needed.

4OA5 Other Activities

.1 Quarterly Resident Inspector Observations of Security Personnel and Activities a. Inspection Scope During the inspection period the inspectors conducted observations of security force personnel and activities to ensure that the activities were consistent with licensee security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities did not constitute any additional inspection samples. Rather, they were considered an integral part of the inspectors' normal plant status reviews and inspection activities.

b. Findings No findings of significance were identified.

4OA6 Management Meetings

.1 Exit Meeting Summary On July 16, 2009 the inspector presented the inspection results to Mr. Ben Waldrep and other members of the licensee staff. The inspectors confirmed that proprietary information was not provided or examined during the inspection period.

Enclosure

An exit meeting for the Heat Sink inspection was conducted on June 5, 2009 with licensee management.

ATTACHMENT: SUPPLEMENTAL INFORMATION Enclosure