ML17333A842: Difference between revisions
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| issue date = 03/12/1997 | | issue date = 03/12/1997 | ||
| title = Responds to NRC 970204 Ltr Re Violations Noted in Insp Repts 50-315/96-13 & 50-316/96-13.Corrective Actions:Instructions Requiring Filter Content Evaluation Removed from Charging Pump Recurring Tasks on 970211 | | title = Responds to NRC 970204 Ltr Re Violations Noted in Insp Repts 50-315/96-13 & 50-316/96-13.Corrective Actions:Instructions Requiring Filter Content Evaluation Removed from Charging Pump Recurring Tasks on 970211 | ||
| author name = | | author name = Fitzpatrick E | ||
| author affiliation = AMERICAN ELECTRIC POWER CO., INC. | | author affiliation = AMERICAN ELECTRIC POWER CO., INC. | ||
| addressee name = | | addressee name = | ||
| Line 15: | Line 15: | ||
| page count = 29 | | page count = 29 | ||
}} | }} | ||
See also: [[ | See also: [[see also::IR 05000315/1996013]] | ||
=Text= | =Text= | ||
Revision as of 13:32, 18 June 2019
| ML17333A842 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 03/12/1997 |
| From: | Fitzpatrick E AMERICAN ELECTRIC POWER CO., INC. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| Shared Package | |
| ML17333A841 | List: |
| References | |
| NUDOCS 9704080224 | |
| Download: ML17333A842 (29) | |
See also: IR 05000315/1996013
Text
Indiana Michigan Power Company 500 Circie D;i'e Bucl anan.III 491071395 INDIANA MICHIGAN POWER March 12, 1997 AEP:NRC:1238F
10 CFR 2.201 Docket Nos.: 50-315 50-316 U.S.Nuclear Regulatory
Commission
ATTN: Document Control Desk Washington, D.C.20555 Gentlemen:
Donald C.Cook Nuclear Plant Units 1 and 2 NRC INSPECTION
REPORTS NOs.50-315/96013(DRS)
AND 50-316/96013 (DRS)REPLY TO NOTICE OF VIOLATIONS
This letter is in response to a letter from G.E.Grant, dated February 4, 1997, that forwarded a notice of three violations
and one notice of deviation to Indiana Michigan Power Company.The violations
and the deviation were identified
during a system operational
performance
inspection (SOPI)of the centrifugal
charging system portion of the emergency core cooling systems and the residual heat removal systems.Our response was due to you on March 6, 1997;however, we requested a brief extension to recover the time delay from when the report was issued to when it was received.The exten'sion
was granted by Ron Gare er of Region III, on February 14, 1997.The three violations
addressed the 1)failure to establish adequate instructions/failure
to follow procedures
as related to collection
of an oil sample, and adequate minimum thread engagement
acceptance
criteria;2)inadequate
test control as related to incorporating
charging pump acceptance
limits into the IST program;and 3)failure to perform adequate/timely
corrective
actions, as related to determining
the correct oil sight-glass
fill marks on safety-related pumps and motors, addressing
equipment deficiency
tagging problems, and locating/reconstituting
a centrifugal
charging pump net positive suction head calculation.
The deviation was from actions committed to in NUREG-0737
specifically
involving the source term used for a radiological
evaluation.
'7704080224
'970403 PDR ADOCK 05000315 8 PDR
4 0
U.S.Nuclear Regulatory
Commission
Page 2 AEP: NRC: 1238F Our reply to the violations
and deviation are provided in the attachment
to this letter.Also included are the results of our review of technical specification
clarifications, which we committed to perform at the December 13, 1996, exit meeting.The reply does not contain any personal privacy, proprietary, or safeguards
information.
Sincerely, PCw p-E.E.Fit patrick Vice President SWORN TO AND SUBSCRIBED
BEFORE ME TH s/X DAY QP)~'997 Notary Public My Commission
Expires: 2/Cr PING/vlb Attachment
JANlCE hl.BIG!<ERS Noey Pub5c, 88men CcunlY, M Qy Q0mmrssc p Eyp;re Fob,<6, 2N$cc: A.A.Blind&3L"%%~8eachh'~:q
MDEQ-DW R RPD NRC Resident Inspector J.R.'adgett
fl'
ATTACHMENT
TO AEP:NRC: 1238F REPLY TO NOTICE OF VIOLATION:
NRC INSPECTION
REPORTS NOs.50-315/96013 (DRS)AND 50-316/96013 (DRS)
Attachment
to AEP:NRC:1238F
Page 1 During an NRC system operational
performance
inspection
conducted November 18 through December 13, 1996, on the emergency core cooling system portion of the centrifugal
charging system and residual heat removal system three violations
and one deviation were identified.
In accordance
with the"General Statement of Policy and Procedures
for NRC Enforcement
Actions," (NUREG-1600)
the violations
and the responses are provided below.Additionally, we were requested to respond to the deviation, and to provide information
related to a commitment
regarding technical specification (T/S)clarifications
made at the December 13, 1996, exit meeting.Our response to these items is also provided below.NRC Violation A"10 CFR 50, Appendix B, Criterion V,'Instructions, Procedures, and Drawings,'equires, in part, that activities
affecting quality shall be prescribed
by instructions, procedures, or drawings of a type appropriate
to the circumstances
and shall be accomplished
in accordance
with these instructions, procedures, or drawings.Maintenance
procedure 12 MHP 5021.001.009, Revision 8,'Torque Selection,'ated
March 21, 1994, requires thread engagement
of at least 80 percent of nut height.Contrary to the above: On December 4, 1996, the i" spectors identified
that a maintenance
work package for the 1E centrifugal
charging pump, an activity af fecting quality,~failed to include adequate instructions
for lube oil sample collection.
On November 20, 1996, the inspectors
identified
that maintenance
procedure MDS-600,'General Erection Tolerances
for Pipe and Tube Supports/Restraints,'as
not of a type appropriate
to the circumstances
since it failed to contain adequate minimum thread engagement
acceptance
criteria for activities
af fecting quality.3.On November 21, 1996, the inspectors
identified
that maintenance
personnel failed to perform bolting on safety-related equipment in accordance
with maintenance
procedure 12MHP5021.001.009,'Torque Selection.'s
a result, nuts associated
with emergency core cooling system equipment were identified
with thread engagement
less than 80 percent of nut height.This a Severity Level IV violation." Res onse to NRC Violation Al 1.Admission or Denial of the Alle ed Violation indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
Reason for the Violation The reason for the violation was failure to remove oil sampling instructions
from applicable
recurring tasks that were no'cnger needed after implementation
of a formal oil sampling program.
,I" tl
Attachment
to AEP:NRC:1238F
Page 2 The instructions
found in the job order activity associated
with the work on the lE centrifugal
charging pump instructed
personnel to: "Drain oil from filter into a container.
A.Deliver oil f rom CUNO f il ter to chem lab for analysis.(The results will go to the engineers for evaluation
of wear in system)." The job order activity instructions
were developed prior to implementation
of our formal oil analysis program.At the time it was input as a recurring task, it was intended to provide a rough indication
of gross machine problems.Subsequently, a formal oil analysis program was implemented, with proceduralized
sampling techniques
being utilized by chemistry personnel.
Under this sampling program, done quarterly (as opposed to filter change-outs
that are done yearly), wear, particles of considerably
less size than those detected via the filter change-out
method can be detected, thus giving much earlier indication
of machine problems.The instructions
in the recurring task were inadvertently
left in place after the formal program was instituted.
The oil collected via these instructions
is not analyzed by chemistry personnel;
and decisions as to the condition of the equipment are not based or.these samples.3.Corrective
Actions Taken and Results Achieved The instructions
requiring filter content evaluation
were removed from the charging pump recurring tasks on February 11, 1997~The 1E charging pump lube oil was sampled by chemistry personnel on September 12, 1996, prior to the filter change-out
observed on December 4, 1996, consistent
with the formal oil analysis program.4.Corrective
Actions Taken to Avoid Further Violations
A:eview of lube oil changes related to equipment included in tne oil analysis program was conducted.
Similar wording was found in recurring tasks for the motor-driven
and turbine-driven auxiliary feedwater pumps.This redundant wording will be removed prior to the next required date for filter change-out
for this equipment.
5.Date When Full Com liance Will Be Achieved Full compliance
was achieved on February 11, 1997, when the redundant instructions
were removed from the four charging pump's recurring.
tasks.Res onse to NRC Violation A2 6 A3 1.Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
Attachment
to AEP:NRC:1238F
Page 3 Reason for the Violation The cause of the violation, as cited in A3, is a combination
of the way work was documented
and adherence to procedural
requirements
that were inconsistent.
The reference to MDS-600, cited in A2, as a"maintenance
procedure" requires clarification.
MDS-600 is not a procedure, it is a design standard that provides tolerances
for installation
and evaluation
of as-found conditions
for piping/tubing
supports.MDS-600 is not an applicable
reference and there is no hierarchial
connection
between MDS-600 and**12 MHP 5021.001.009.
3.Corrective
Actions Taken and Results Achieved Eight condition reports were written to document the inspection
team's concerns.Operability
reviews were performed based on the identified
deficiencies, and the affected equipment was determined
to be operable.Work history for each component was reviewed to assist in determining
the potential cause(s).In general, this review identified
a general time frame when the deficiency
was created, but not a specific work activity.Action requests were written to correct the deficiency
where an action request did not already exist, or the deficiency
was evaluated and found to be acceptable
as is.4.Corrective
Actions Taken to Avoid Further Violations
Maintenance
standing order, MSO.009, was issued on February 3, 1997.This document establishes
an acceptance
criteria of"flush or better" for thread engagement.
Further, it provides a policy for documenting
as-found thread engagement
deficiencies
so they can be evaluated and corrected.
Lastly, the policy provides for in-plant identification
of less than flush thread engagement
that has been evaluated and found to be acceptabl.This standing order strengthens
management
expectations
for thread engagement
and establishes
a mechanism for identification
of analyzed, acceptable
conditions.
A walkdown was performed of a random sample of plant components
of sufficient
size to provide a 99%confidence
level that these components
are a statistically
valid sample of the plane population
of components.
The as-found configuration
of the fasteners associated
with these components
was evaluated.
There were no fastener anomalies identified
that affected component functionality
or operability.
Plant management
has reinforced
procedural
adherence to all plant personnel.
- 12 MHP 5021.001.009 was enhanced by the addition of acceptance
criteria of flush threads or better.
I
Attachment
to AEP:NRC.:1238F
5.Date When Full Com liance Will Be Achieved Page 4 Full compliance
was achieved on March 10, 1997.At that time the original 28 NRC-identified
thread engagement
deficiencies
were analyzed as not affecting operability/quality;
existing procedures, policies, and standards were upgraded;and the findings of the thread engagement
random sample concluded that there were no functionality/operability
concerns caused by thread engagement
deficiencies
associated
with any of the sampled components.
NRC Violation B"10 CFR 50, Appendix B, Criterion XZ,'Test Control,'equires, in part, that a test program be established
to assure that all testing required to demonstrate
that structures, systems, and components
will perform satisfactorily
in service is identified
and performed in accordance
with written test procedures
which incorporate
the requirements
and acceptance
limits contained in applicable
design documents.
Technical Specification 3.1.1.1,'Shutdown Margin-Tave greater than 200'F,'pecifies
a boration capability
of 10 gallons per minute (gpm)of 20,000 parts per million (ppm)boron solution or equivalent.
Contrary to the above, on December 11, 1996, the inspectors
identified
that the correct acceptance
limits to assure that the centrifugal
charging pumps could perform their boron injection function as specified in Technical Specification 3.1.1.1 had not been incorporated
in the licensee's
inservice testing (ZST)program.This is a Severity Level ZV violation." Res onse to NRC Violation B Admission or Denial of the Alle ed Violation Zndiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
2.Reason'for the Violation The reason for the violation was that a review to determine applicability
to the ZST program was not conducted prior to issuance of a technical specification (T/S)clarification
on T/S 3.1.1.1.T/S 3.1.1.1, Shutdown Margin-T,~greater than 2004F provides shutdown margin requirements
while in modes 1, 2, 3, or 4.The action statement for T/S 3.1.1.1 requires immediate and continuous
boration at greater than or equal to 10 gpm of a solution containing
greater than or equal to 20,000 ppm boron or"equivalent".
performed an analysis to clarify the meaning of this statement if the refueling water storage tank (RWST)was used as a source of borated water.Westinghouse
defined"equivalence" as"xenon burnout equivalence", which is the capability
to inject sufficient
boron to adjust aoron concentration
to compensate
for xenon burnoutfrom its peak value Their analysis assumed a plant trip followed by a step return to 100%.power
Attachment
to AEP:NRC:1238F
Page 5 at peak xenon concentration.
Zn addition, they assumed that the reactor would be maintained
at full power during the transient.
The results of this analysis showed that a centrifugal
charging pump (CCP)flow of 120 gpm from the RWST could compensate
for xenon throughout
the transient if certain restrictions
were observed.On November 5, 1990, a revision to T/S clarification
no.7 was issued, which defined the 120 gpm of RWST water containing
2400 ppm boron as an acceptable
source of water to satisfy boration flow requirements
for T/S 3.1.1.1.Development
and issuance of this T/S clarification
was not coupled with a review of the test program to ensure the test program confirmed the ability of the CCPs to perform this function.This deficiency
was identified
by our engineers during efforts to respond to an inspector's
question on the design functions of the CCPs during the inspection.
Corrective
Actions Taken and Results Achieved Following identification
of this deficiency, a calculation
was performed to determine the maximum degradation
the CCPs could tolerate while still~eing able to deliver 120 gpm of RWST water to the reactor coolant system.This calculation
revealed that the CCPs could tolerate a degradation
of 9.5%for Unit 1 and 3.5%for Unit 2.A review of ZST data as far back as 1990 determined
that the pumps were capable of performing
this function.The ZST program has been revised to include limitations
for allowable degradation
of the CCPs to ensure that 120 gpm of 2400 ppm boron could be supplied from the RWST.Additionally, as a point of information, since the original analysis by Westinghouse, which defined the 120 gpm value of 2400 ppm boron included a very conservative
assumption
that a step increase in power to 100%occurred while at peak xenon, a reanalysis
was performed using a more realistic ramp rate of 10'k/hr, which is a limitation
contained in plant procedures.
This reanalysis
indicated that the boration flow requirements
of T/S 3.1.1.1 could be satisfied by as little as 60.1 gpm of 2400 ppm boron.We may relax the allowable degradation
for the CCPs based on this revised 60.1 gpm flow.Corrective
Actions Taken to Avoid Further Violations'ailure
to ensure the test program for the CCPs included provisions
to ensure the CCPs could deliver 120 gpm of 2400 ppm boron occurred as a result of failure to couple the development
and issuance of a T/S clarification
with appropriate
reviews of the test program.As noted in the SOPZ report, several examples were identified
where T/S clarifications
could not be justified.
During the exit meeting, we committed to perform a review of all of our T/S clarifications.
The results of this review are contained in the"Commitment"'ection of this attachment.
Additionally, as noted, improvements
will be made in the T/S clarificaticn
review process to ensure an adequate technical review of future clarifications.
Attachment
to AEP:NRC: 1238F Page 6 Date When Full Com liance Will Be Achieved Full compliance
was achieved on December 18, 1996, when the IST program was revised to include appropriate
limits to ensure that each units'CPs can supply 120 gpm of 2400 ppm boron from the RWST.Violation C"10 CFR 50, Appendix B, Criterion XVI,'Corrective
Actions,'equires, in part, that measures shall be established
to assure that conditions
adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformances
are promptly identified
and corrected.
Contrary to the above: 2.3.Corrective
actions to address potentially
inaccurate
sight-glass fill marks for safety-related
pumps and motors, a condition adverse to quality, were not initiated until November 27, 1996, although in 1995 job orders were written to address potentially
inaccurate
sight-glass
fill marks on safety-related
pumps and motors, and on March 6, 1996, an action request was written to determine correct sight-glass
fill marks on safety-related.
pumps and motors.On December 5, 1996, the inspectors
identified
that the licensee failed to take corrective
actions to either locate or re-constitute
a centrifugal
charging pump net positive suction head (NPSH)calculation
although the calculation
had been identified
as missing about 18 months earlier.On December 4, 1996, the inspectors
determined
that the licensee failed to take timely corrective
actions to address equipment deficiency
tagging problems.Although the licensee had identified
that about 30 percent of plant components
in the work'control
system reviewed in a three week period were not properly tagged in the field, corrective
actions to a iress this concern had not been initiated.
This is a Severity Level IV violation." Res onse to NRC Violation Cl Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
2.Reason for the Violation The cause of the untimely response for guidance on plant pump/motor
oil fill levels was the lack of a communication
protocol resulting in an unrecognized
request to engineering
personnel from operations
personnel for technical assistance.
The request for assistance
was made by means of an action request.Requests for engineering
direction are made within the nuclear plant maintenance (NPM)computer system by means of an evaluation
request.Different searches are required to locate action requests and evaluation
requests.Engineering
personnel did not search action requests because they were not an expected means for requesting
assistance.
Attachment
to AEP:NRC:1238F
Page 7 The request for guidance on plant pump/motor
oil fill levels was brought to engineering
management's
attention approximately
five months after the action-equest was initiated.
At that time engineering
personnel began work to provide the requested guidance.The background
research was completed and the guidance issued on December 5, 1996.Corrective
Actions Taken and Results Achieved The requested information
on pump/motor
oil fill levels was provided on December 5, 1996.A search of action requests assigned to engineering
personnel has been performed to ensure the responsible
groups are aware of assignments.
Additionally, as an interim action, plant personnel have been instructed
to make daily searches to ensure no new action requests for engineering
assistance
go unrecognized.
4, Corrective
Actions Taken to Avoid Further Violations
An acceptable
method for requesting
engineering
assistance
will be developed by March 21, 1997'.Date When Full Com liance Will Be Achieved Full compliance
was achieved on December 5, 1996, when the requested technical guidance was provided.Res onse to NRC Violation C2 Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
2.Reason for the Violation In June 1995, as part of the design basis documentation (DBD)program, it was identified
that the NPSH calculation
for the CCPs cauld not be located.A DBD action item was init'ated in accordance
with DBD program procedures.
This item was classified
as an instance of a"missing reference document", a categorization
with a normal resolution
time of 60 days.Engineering
personnel involved in the classification
of this item were aware that an NPSH calculation
for the CCPs had been performed at one time,.even though it could not be located.Operability
was not considered
to be a concern because it was known that the calculation
had been performed but could not be found.Therefore, a high priority was not placeu on reconstituting
the calculation
or resolving the DBD action item.Corrective
Actions Taken and Results Achieved As noted in the SOPI report, a new calculation
was completed prior to and approved during the SOPI inspection, which confirmed adequate NPSH to the CCPs.Corrective
Actions Taken to Avoid Further Violations
Following the SOPI inspection, a review of all open DBD action items was performed, by January 15, 1997, to assess
0
Attachment
to AEP:NRC: 1238F Page 8 the appropriateness
of their classification.
A series of additional
DBD action items were formally entered into the corrective
action system (via condition reports)as a result of this review.The corrective
action system includes requir'ements
for determining
operability
in a timely manner.Entry into the corrective
action system ensures a review of these issues by our condition assessment
group (CAG).In its oversight function, the CAG assesses the need and makes assignments
for confirmatory
operability
determinations
or supplemental.
analysis.Beginning in January 1997, additional
resources were added to the DBD project to enable prompt closure of DBD action items.Specifically, the DBD project manager position, which had been vacant since September 1996, was filled and two additional
utility personnel and two contract personnel were assigned to the project.These personnel are aggressively
pursuing, resolution
of open DBD'action items.This augmentation
of personnel will.continue through late 1997, by which time we expect to have made significant
progress in the closure of DBD action items.Additionally, we are training members of our staff, who have ownership of the DBDs, to ensure they understand
the importance
of promptly resol"ing DBD action items and also to ensure they clearly understand
the process for effecting closure of these items.This training commenced in early February 1997 and will be completed by March 15, 1997.Finally, the DBD action item review process is being strengthened
to limit the number of ava.'lable
classifications
for DBD action items and also to ensure a more comprehensive
review of action items by appropriate
personnel.
Project instructions
related to action item processing
are being revised.These revisions will be completed by March 28, 1997.Date When Full Com liance Will Be Achieved Full compliance
was achieved on December 2, 1996, when a new calculation
was approved which confirmed adequate NPSH to the CCPs.Res onse to NRC Violation C3 Admission or Denial of the Alle ed Violation Indiana Michigan Power Company admits to the violation as cited in the NRC notice of violation.
2.Reason for the Violation The primary reason for the violation is that plant personnel were not sufficiently
aware of the guidance regarding when to hang deficiency
tags for corrective
maintenance.
This was further compounded
by the lack of clarity provided by the administrative
requirements
that def ine def i-iency tag hanging requirements.
Further, condition reports were not generated when missing deficiency
tags were identified
to prompt appropriate
actions via the plant's,corrective
action program.While written
Attachment
to AEP:NRC:1238F
Page 9 memoranda identifying
the missing deficiency
tags were generated, condition reports were not written and therefore, appropriate
attention and follow-through
were not instituted.
Zn all cases evaluated, the work control process had captured the identified
degraded component, ensuring that the deficient condition would be corrected in a timely manner.Corrective
Actions Taken and Results Achieved Recent plant management
actions have been taken to improve focus on promptly identifying
problems and corrective
actions dealing-with conditions
adverse to plant requirements.
A condition report was promptly written when the NRC noted the lack of timely corrective
action to address the identified
deficiency
tagging issue.The condition report 1)proposes that the material condition group replace missing tags when discovered, 2)recommends
changes to the governing document NPM-02CM, and 3)requests assistance
from computer personnel to modify existing NPM software to better support the rehanging of tags.The personnel responsible
for ident'ying
missing deficiency
tags were coached on the expectation
to generate additional
condition reports in the future.Corrective
Actions Taken to Avoid Further Violations
By April 1, 1997, the governing document.detailing when and how to tag deficiencies
will be revised and appropriate
personnel will be made aware of"the revised requirements.
Also, as of April 1, 1997, action requests generated that have not met the revised deficiency
tagging requirements
will be returned to the originating
personnel for resolution
before the action request will be processed further.By September 1, 1997, system walkdowns will have been performed to verify that deficiency
tags associated
with existing corrective
maintenance
action requests (those generated before April 1, 1997), comply with the revised requirements.
Date When Full Com liance Will Be Achieved Full compliance
will be achieved by April 1, 1997, when the deficiency
tagging requirements
have been revised and appropriate
personnel have been made aware of those requirements.
Further, condition reports will be written as of April 1, 1997, for any deficiency
tag not in compliance
with the revised requirement (regardless
of when the action request and associated
deficiency
tags were generated).
)I'
Attachment
to AEP:NRC:1238F
Deviation Page 10 In addition to the above three violations, the notice of violation contained'the following notice of deviation, which is addressed below.DEV 50-315 96013-09 DRS and DEV 50-316 96013-09 DRS'"During an NRC inspection
conducted November 18 through December 13, 1996, a deviation of your actions committed to in NUREG-0737, Section IZ.B.2 was identified.
In accordance
with the'General Statement of Policy and Procedures
for NRC Enforcement
Actions,'UREG-1600, the deviation is listed below: NUREG-0737, Section ZI.B.2,'Design Review of Plant Shielding and Environmental
Qualification
of Equipment for Spaces/Systems
Which May Be Used in Postaccident
Operations,'equires
that 50 percent of the total iodine and 100 percent of the noble gases are assumed to be released from the fuel~in the design basis accident radiological
analysis.Contrary to the above, on December 4, 1996, the inspectors
identified
that the licensee failed to correctly translate Section ZZ.B.2 of NUREG-07~7
into the centrifugal
charging pump emergency leakoff valve failure design basis accident radiological
analysis.As a result, only one percent fuel damage was assumed in the analysis and resulted in dose estimates lower than revised calculated
values." Res onse to NRC Deviation Reason for the Deviation In August 1991, a small break loss of coolant accident scenario run on the plant simulator identified
a flowpath that had the potential to divert water away from the emergency core cooling system and containment
building.The flowpath was from the safety injection system (SIS)ce trifugal charging pump discharge through an emergency leakof f valve, through the reactor coolant pump (RCP)seal return line safety valve to the volume control tank (VCT)and through the VCT safety valve to the chemical and volume control system holdup tanks.This condition was documented
in LER 91-007-00.
A review was conducted to assess the safety consequence
and implications
of the postulated
event.Analysis of the potential dose rate from the diverted water to the whole body at the site boundary was calculated
to be insignificant
compared to the 10 CFR 100 accident dose limit and even with the 10 CFR 20.105 dose limits for unrestricted
areas during normal operations, based on the assumption
of 1%failed fuels LER 91-007-01 provided original corrective
action for this scenario.The scenario of concern occurs following the switchover
of the CCP suction from the refueling water storage tank to the recirculation
sump via the residual heat removal (RHR)pumps.With the RHR pumps supplying suction to the CCPs, the pressure in the CCP emergency leakoff (ELO)lines could be in excess of the downstream
safety valve set pressure, and then approximately
60 gpm flow would be diverted from the ECCS to the VCT.Corrective
actions for this scenario included emergency operating procedure (EOP)
Attachment
to AEP:NRC:1238F
Page 11 modifications
to close the charging pump ELO valves as part of the switchover
from injection to recirculation
phase where the ECCS pumps take suction from the recirculation
sump.In June 1995, as part of our DBD program, it was identified
that the EOPs noted above can be implemented, but were not single failure proof.The DBD program includes a process to identify, classify (with respect to safety significance), and resolve action items identified
during the development
was created to document that in the event the single failure is an ELO valve that'cannot be isolated, the leakage path to the VCT would still persist.Within the DBD program, this issue was classified
as a discrepancy
that was not safety significant, based on the analysis described, above and documented
in LER 91-007.The reliance on the prior analysis in LER 91-007, which provided a practical assessment
of safety significance
per 10 CFR 50.73, to classify the DBD action item as a non-significant
discrepancy
was incorrect because it did not consider design basis assumptions
for source term per NUREG-0737.
The misclassification
of the DBD action item was made by engineering
personn 1 who incorrectly
assumed that the analysis presented in LER 91-007 was also an adequate basis for classification
of th DBD action item.2.Corrective
Actions Taken and Results Achieved The EOPs have been modified to inst uct the operator to turn off a CCP for which the ELO valve cannot be closed.Flow through the idle pump of up to 5.2 gpm may still exist;therefore, instructions
have been added to isolate the valve manually.(The 5.2 gpm is within the 10 gpm value f or outside containment
leakage previously
evaluated and determined
acceptable
regarding offsite and control room doses.)The maximum dose'to personnel expected to isolate the valve is 0.28 rem 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after the accident occurs.3.Correcti re Action's Taken to Avoid Further Deviations
Following the SOPI inspection, a review of all open DBD action items was completed on January 15, 1997, to assess the appropriateness
of their previous classification.
A series of additional
DBD action items were formally entered into the corrective
action system as a result of this review.Entry into the corrective
action system ensures a thorough screening of these issues by the CAG for assignment
to the appropriate
organization
for resolution.
The corrective
action system includes requirements
for determining
operability
in a timely manner.In its oversight function, the CAG asse'sses the need and makes assignments
for confirmatory
operability
determinations
or supplemental
analysis.The DBD action item review process is being strengthened
to limit the number of available classifications
for DBD action items and also to ensure a more comprehensive
review of action items by appropriate
personnel.
Project instructions
related to action item processing
are being revised.These revisions will be completed by March 28, 1997.
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4.Date When Full Com liance Will Be Achieved Page 12 Corrective
action was completed on December 13, 1996, when changes"ere made to the EOPs to instruct the operator to turn off a CCP for which the ELO valve cannot be closed.
Attachment
to AEP:NRC:1238F
Page 13 Commitment
The inspection
report requested we respond in writing regarding our review of T/S clarifications.
The notice of violation contained the following discussion."The licensee had 37 technical specification
clarifications (TSCs)in effect.The inspectors
reviewed the TSCs listed below and questioned
whether the licensee could provide technical justification
to support the TSCs.Subsequently, the licensee determined
that the following clarifications
could not be technically
justified and should be canceled: TSC¹14 TSC¹l5 TSC¹48 Airborne Radioactivity
Monitor Operability
Diesel Generator Surveillance
Runs-Paralleled.
Grid Technical specification (TS)4.8.1.1.2.F.2
Leak Testing of AD and CD Fuel Oil Tanks and Associated
Piping The inspectors
did not identify any past use of the above TSCs that resulted in exceeding the action requirements
of the associated
technical specification.
The inspectors
concluded that the safety significance
of the TSC errors were minimal.The inspectors
concluded that the licensee's
approval of TSCs without appropriate
technical justification
was a weakness.At the end, of the inspection, the licensee committed to review all remaining TSCs to ensure they were still necessary and could be justified." Review Sco e The NRC inspection
report indicated that 37 TSCs were in effect at the time of the inspection.
A review of the active TSCs from the, TSC index indicated that there were actually 35 active TSCs.The three TSCs discussed in the inspection
report were canceled.The scope of the TSC review was of the remaining 32 active TSCs.Observation
and Findin s Nine TSCs were canceled They are as follows TSC¹5 TSC¹12 TSC¹26 TSC¹37 TSC¹38 TSC¹45 TSC¹47 TSC¹60 TSC¹61 Operable-Operability
Definition
-Attendant Xnstrumentation
D.C.Distribution
-Operating Steam Generator Stop Valve Operability
Definition
of Maintenance
on Emergency Core Cooling System Valves Turbine Driven Auxiliary Feedwater Pump Operability
Snubber Functional'est
Retest Results 10 CFR 50 Appendix R Equipment Operability
Auxiliary Feedwater System and Essential Service Water System Auxiliary Feedwater System Surveillance
Requirements
Of this group, two TSCs (¹5 and¹12), were canceled due to insufficient
technical bases to support the implied operability
provided by the TSC.Three TSCs (¹37,¹60 and¹61)were canceled
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Page 14 as they were implemented
in a manner inconsistent
with current expectations.
Four TSCs (¹26,¹38,¹45 and¹47)were determined
to be unnecessary.
One TSC (¹65), boric acid transfer pump operability, was revised to properly reflect its technical bases (refer to section 08.1 of the NRC inspection
report).The remaining 22 TSCs remain active.Conclusion
Based on the review of the existing TSCs, it follows that the TSCs were not well defined and were implemented
in a manner inconsistent
with current expectations.
The, program was utilized to capture many event driven decisions that would more appropriately
fit an operability
program, or should be translated
into approved procedural
controls.An improved TSC program will be developed by June 27, 1997.This program will provide a review of proposed new clarifications
to ensure adequate technical justification
is present prior to approval, and that a clarification
does not change or alter the requirement
of the specification
being clarified.
Additionally, the new program will reg'uire plant impact reviews as part of the implementation
process.The impact reviews will ensure appropriate
review and incorporation
of clarification
information
into plant procedures
and programs'he
impact review process is being incorporated
into the implementation
process to address a SOPI concern involving integration
of TSC¹7 into the plant's IST program.