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{{Adams|number = ML080080622}} | {{Adams | ||
| number = ML080080622 | |||
| issue date = 01/08/2008 | |||
| title = IR 05000298-07-010; 12/03/07 - 12/06/07; Cooper Nuclear Station. Inspection Procedure Supplemental Inspection | |||
| author name = Hay M C | |||
| author affiliation = NRC/RGN-IV/DRP/RPB-C | |||
| addressee name = Minahan S B | |||
| addressee affiliation = Nebraska Public Power District (NPPD) | |||
| docket = 05000298 | |||
| license number = DPR-046 | |||
| contact person = | |||
| document report number = IR-07-010 | |||
| document type = Inspection Report, Letter | |||
| page count = 16 | |||
}} | |||
{{IR-Nav| site = 05000298 | year = 2007 | report number = 010 }} | {{IR-Nav| site = 05000298 | year = 2007 | report number = 010 }} | ||
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NRC Inspection Report 05000298/2007010 Nebraska Public Power District- 2 -cc: w/enclosures:Gene Mace Nuclear Asset Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321John C. McClure, Vice President and General Counsel Nebraska Public Power District P.O. Box 499 Columbus, NE 68602-0499David Van Der Kamp Licensing Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321Michael J. Linder, DirectorNebraska Department of Environmental Quality P.O. Box 98922 Lincoln, NE 68509-8922ChairmanNemaha County Board of Commissioners Nemaha County Courthouse 1824 N Street Auburn, NE 68305Julia Schmitt, ManagerRadiation Control Program Nebraska Health & Human Services Dept. of Regulation & Licensing Division of Public Health Assurance 301 Centennial Mall, South P.O. Box 95007 Lincoln, NE 68509-5007H. Floyd GilzowDeputy Director for Policy Missouri Department of Natural Resources P. O. Box 176 Jefferson City, MO 65102-0176 Nebraska Public Power District- 3 -Director, Missouri State Emergency Management Agency P.O. Box 116 Jefferson City, MO 65102-0116Chief, Radiation and Asbestos Control Section Kansas Department of Health and Environment Bureau of Air and Radiation 1000 SW Jackson, Suite 310 Topeka, KS 66612-1366Melanie Rasmussen, State Liaison Officer/ Radiation Control Program Director Bureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5th Floor 321 East 12th Street Des Moines, IA 50319John F. McCann, Director, LicensingEntergy Nuclear Northeast Entergy Nuclear Operations, Inc. | NRC Inspection Report 05000298/2007010 Nebraska Public Power District- 2 -cc: w/enclosures:Gene Mace Nuclear Asset Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321John C. McClure, Vice President and General Counsel Nebraska Public Power District P.O. Box 499 Columbus, NE 68602-0499David Van Der Kamp Licensing Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321Michael J. Linder, DirectorNebraska Department of Environmental Quality P.O. Box 98922 Lincoln, NE 68509-8922ChairmanNemaha County Board of Commissioners Nemaha County Courthouse 1824 N Street Auburn, NE 68305Julia Schmitt, ManagerRadiation Control Program Nebraska Health & Human Services Dept. of Regulation & Licensing Division of Public Health Assurance 301 Centennial Mall, South P.O. Box 95007 Lincoln, NE 68509-5007H. Floyd GilzowDeputy Director for Policy Missouri Department of Natural Resources P. O. Box 176 Jefferson City, MO 65102-0176 Nebraska Public Power District- 3 -Director, Missouri State Emergency Management Agency P.O. Box 116 Jefferson City, MO 65102-0116Chief, Radiation and Asbestos Control Section Kansas Department of Health and Environment Bureau of Air and Radiation 1000 SW Jackson, Suite 310 Topeka, KS 66612-1366Melanie Rasmussen, State Liaison Officer/ Radiation Control Program Director Bureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5th Floor 321 East 12th Street Des Moines, IA 50319John F. McCann, Director, LicensingEntergy Nuclear Northeast Entergy Nuclear Operations, Inc. | ||
440 Hamilton Avenue White Plains, NY 10601-1813Keith G. Henke, PlannerDivision of Community and Public Health Office of Emergency Coordination 930 Wildwood, P.O. Box 570 Jefferson City, MO 65102Paul V. Fleming, Director of Nuclear Safety Assurance Nebraska Public Power District P.O. Box 98 Brownville, NE 68321Ronald L. McCabe, ChiefTechnological Hazards Branch National Preparedness Division DHS/FEMA 9221 Ward Parkway Suite 300 Kansas City, MO 64114-3372 Nebraska Public Power District- 4 -Daniel K. McGhee, State Liaison OfficerBureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, | 440 Hamilton Avenue White Plains, NY 10601-1813Keith G. Henke, PlannerDivision of Community and Public Health Office of Emergency Coordination 930 Wildwood, P.O. Box 570 Jefferson City, MO 65102Paul V. Fleming, Director of Nuclear Safety Assurance Nebraska Public Power District P.O. Box 98 Brownville, NE 68321Ronald L. McCabe, ChiefTechnological Hazards Branch National Preparedness Division DHS/FEMA 9221 Ward Parkway Suite 300 Kansas City, MO 64114-3372 Nebraska Public Power District- 4 -Daniel K. McGhee, State Liaison OfficerBureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5 th Floor321 East 12 th StreetDes Moines, IA 50319Ronald D. Asche, President and Chief Executive Officer Nebraska Public Power District | ||
1414 15 th StreetColumbus, NE 68601 Nebraska Public Power District- 5 -Electronic distribution by RIV:Regional Administrator (EEC)DRP Director (DDC)DRS Director (RJC1)Senior Resident Inspector (NHT)Branch Chief, DRP/C (MCH2)Senior Project Engineer, DRP/C (WCW)Team Leader, DRP/TSS (CJP)RITS Coordinator (MSH3)DRS STA (DAP)D. Pelton, OEDO RIV Coordinator (DLP)ROPreports CNS Site Secretary (SEF1)SUNSI Review Completed: __WCW____ADAMS: Yes G No Initials: _WCW Publicly Available G Non-Publicly Available G Sensitive Non-SensitiveR:\_REACTORS\CNS\2007\CNS95001IR.wpdRIV:SPE/CC:DRP/CWCWalkerMCHay/RA//RA/12/13/071/8/08OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax EnclosureU.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket:50-298License:DPR-46 Report:05000298/2007010 Licensee:Nebraska Public Power District Facility:Cooper Nuclear Station Location:Brownville, Nebraska Dates:December 3 through December 6, 2007 Inspector:W. C. Walker, Senior Project Engineer, Branch C, Division of ReactorProjects (DRP)Approved By:M. C. Hay, Chief, Project Branch C, DRP ATTACHMENT:Supplemental Information Enclosure-2-SUMMARY OF FINDINGSIR05000298/2007010; 12/03/2007 - 12/06/2007; Cooper Nuclear Station. Inspection Procedure95001 Supplemental Inspection.The report covered a one-week period of inspection by a region-based inspector. No violationswere identified. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.Cornerstone: Mitigating Systems The U.S. Nuclear Regulatory Commission performed this supplemental inspection to assessthe licensee's evaluations of emergency diesel generator equipment problems associated witha performance indicator (Emergency AC Power) that crossed the Green-White threshold in the first quarter of 2007 and a related White finding involving inadequate corrective actions documented in NRC Inspection Report 05000298/2007007(ADAMS ML072290167). During this supplemental inspection, performed in accordance with Inspection Procedure 95001, the inspector determined that the licensee performed comprehensive evaluations of the three diesel generator failures that occurred since 2004. Specifically, the following three events contributed to the White performance indicator: 1) a lube oil sensing line leak in 2004 causing a failure of the diesel to run, 2) a control power failure in 2005 causing a diesel failure to start, and 3) a faulty voltage regulator circuit board in 2007 causing a diesel failure to run. On the basis of the licensee's evaluations for the above events the inspector determined that the primary root causes and corrective actions for the above performance issues were appropriately evaluated and implemented. In addition to the above issues a White finding was also identified for the January 2007 dieselfailure involving inadequate corrective actions related to repeat failures of the diesel generator voltage regulator circuit board. The licensee identified that the procedure for elevating repeat occurrences of problems to a root cause evaluation was inadequate. This deficiency resulted in the licensee's failure to perform a root cause evaluation following repetitive problems experienced with the emergency diesel generator voltage regulator circuit board following its installation. The root cause of the January 2007 event was determined to be: 1) a manufacturing defect of a zener diode on the voltage regulator circuit board, and 2) the process for maintaining quality of replacement safety-related components did not include the evaluation of operating experience for vendors removed from the approved suppliers list. Corrective actions to address the White finding included: 1) new procedures requiring burn in of electrical components were instituted, 2) a comprehensive review of all safety-related parts in the warehouse was conducted with holds placed on any parts that required further evaluation, and 3) the condition report procedure for escalation of repeat issues in the corrective action program was revised.Given the licensee's acceptable performance in addressing the diesel failures, the white findingassociated with this issue will only be considered in assessing plant performance for a total of four quarters in accordance with the guidance in Inspection Manual Chapter (IMC) 0305, | |||
"Operating Reactor Assessment Program." Since the White finding was documented in the second calendar year quarter of 2007 the finding will remain in effect until the end of the first calendar year quarter of 2008. | "Operating Reactor Assessment Program." Since the White finding was documented in the second calendar year quarter of 2007 the finding will remain in effect until the end of the first calendar year quarter of 2008. | ||
Enclosure-3-Report | Enclosure-3-Report Details 01INSPECTION SCOPEThe U.S. Nuclear Regulatory Commission performed this supplemental inspection toassess the licensee's evaluation associated with a performance indicator (Emergency AC Power) that crossed the Green-White threshold in the first quarter of 2007. The primary reason for this performance indicator being characterized as White was a second run failure of the emergency diesel generators in a 36 month period, on January 18, 2007. Overall, the Mitigating Systems Performance Index (MSPI) for the Emergency AC Power function represents three actual failures of the emergency diesel generators. This performance results in a change in core damage frequency that is characterized by industry standards as risk significant. An MSPI value of 5.7E-06/year was calculated for the three failures which exceeded the risk significance threshold of 3.4E-06/year as established by the industry and NRC. The change in core damage frequency resulting from the three failures represented by the emergency AC power MSPI value is characterized by the Reactor Oversight Process as a performance level that crosses the Green-White threshold. In addition to the White performance indicator the NRC staff also identified a Whitefinding and determined a corrective action violation occurred. The licensee failed to promptly identify a significant condition adverse to quality that resulted in reduced reliability of emergency diesel generator (EDG) 2. Two distinct and reasonable opportunities to identify the condition adverse to quality existed yet the condition was not promptly identified and corrected to preclude recurrence. Specifically, inadequate procedural guidance for evaluating the suitability of parts used in safety related applications presented one missed opportunity to identify that an EDG voltage regulating circuit board was defective prior to installation on November 8, 2006. | ||
Following installation of the defective EDG 2 voltage regulator circuit board two high voltage conditions, one resulting in an EDG automatic high voltage trip, occurred on November 13, 2006. The licensee's evaluation of these high voltage events missed another opportunity to identify and correct the deficient condition. The failure to identify and correct this deficient condition resulted in an additional high voltage trip of EDG 2 that occurred on January 18, 2007. During this supplemental inspection, performed in accordance with InspectionProcedure 95001, the inspector determined that the licensee adequately determined the root causes and significant contributing causes of the Mitigating Systems Performance Index for Emergency AC Power crossing the Green-White threshold and the White finding for inadequate corrective actions, and established appropriate corrective actions to prevent recurrence. | Following installation of the defective EDG 2 voltage regulator circuit board two high voltage conditions, one resulting in an EDG automatic high voltage trip, occurred on November 13, 2006. The licensee's evaluation of these high voltage events missed another opportunity to identify and correct the deficient condition. The failure to identify and correct this deficient condition resulted in an additional high voltage trip of EDG 2 that occurred on January 18, 2007. During this supplemental inspection, performed in accordance with InspectionProcedure 95001, the inspector determined that the licensee adequately determined the root causes and significant contributing causes of the Mitigating Systems Performance Index for Emergency AC Power crossing the Green-White threshold and the White finding for inadequate corrective actions, and established appropriate corrective actions to prevent recurrence. | ||
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Enclosure-8-b.Prioritization of corrective actionsThe inspector did not identify any specific methods utilized to prioritize the specifiedcorrective actions based on risk significance or regulatory compliance. However, no examples of inappropriate prioritization were noted. The inspector considered the prioritization of the established corrective actions to be consistent with risk consequences.c.Establishment of schedule for implementing and completing the corrective actionsThe licensee established adequate schedules for completion of the specified correctiveactions. As appropriate, some corrective actions were tied to scheduled equipment outages while others were more short term such as procedure revisions or training updates. The inspector did not identify any specific concerns with the scheduling orcompletion of established corrective actions. The inspector did note that the diesel generator improvement plan regarding long termreliability improvements for the emergency diesel generators was included as a corrective action to be tracked in condition report CR-CNS-2007-01559. The inspector considered this initiative to be appropriate and should assist the licensee in the stated goal of the improvement plan to increase EDG reliability, availability, and maintenance predictability.d.Establishment of quantitative or qualitative measures of success for determining theeffectiveness of the corrective actions to prevent recurrenceThe licensee implemented a maintenance procedure change to the diesel generatorelectrical examination and maintenance procedure. This change included increased tasks to verify terminal tightness on diesel electrical equipment and perform thermography as a diagnostic tool to identify potential electrical problems in the EDGs prior to failure. The inspector interviewed station personnel involved in this effort and determined that this change had been implemented and was in use. The maintenance procedure specified the method, success criteria, and timing of this action in specific terms. The inspector identified no concerns in this area.The licensee also established controls on all safety-related parts in the warehouse toensure any parts that were not supported by documentation that ensured the parts were approved under an approved supplier program were placed on hold. The inspector reviewed this program and considered it appropriate to ensure only qualified safety- | Enclosure-8-b.Prioritization of corrective actionsThe inspector did not identify any specific methods utilized to prioritize the specifiedcorrective actions based on risk significance or regulatory compliance. However, no examples of inappropriate prioritization were noted. The inspector considered the prioritization of the established corrective actions to be consistent with risk consequences.c.Establishment of schedule for implementing and completing the corrective actionsThe licensee established adequate schedules for completion of the specified correctiveactions. As appropriate, some corrective actions were tied to scheduled equipment outages while others were more short term such as procedure revisions or training updates. The inspector did not identify any specific concerns with the scheduling orcompletion of established corrective actions. The inspector did note that the diesel generator improvement plan regarding long termreliability improvements for the emergency diesel generators was included as a corrective action to be tracked in condition report CR-CNS-2007-01559. The inspector considered this initiative to be appropriate and should assist the licensee in the stated goal of the improvement plan to increase EDG reliability, availability, and maintenance predictability.d.Establishment of quantitative or qualitative measures of success for determining theeffectiveness of the corrective actions to prevent recurrenceThe licensee implemented a maintenance procedure change to the diesel generatorelectrical examination and maintenance procedure. This change included increased tasks to verify terminal tightness on diesel electrical equipment and perform thermography as a diagnostic tool to identify potential electrical problems in the EDGs prior to failure. The inspector interviewed station personnel involved in this effort and determined that this change had been implemented and was in use. The maintenance procedure specified the method, success criteria, and timing of this action in specific terms. The inspector identified no concerns in this area.The licensee also established controls on all safety-related parts in the warehouse toensure any parts that were not supported by documentation that ensured the parts were approved under an approved supplier program were placed on hold. The inspector reviewed this program and considered it appropriate to ensure only qualified safety- | ||
related parts would be placed in the plant.03MANAGEMENT MEETINGSExit Meeting SummaryOn December 6, 2007, the inspector presented the inspection results to Mr. S. Minahan, VicePresident-Nuclear and CNO, and members of his staff who acknowledged the findings. The inspector confirmed that no proprietary information was provided or examined during the inspection. | related parts would be placed in the plant. | ||
03MANAGEMENT MEETINGSExit Meeting SummaryOn December 6, 2007, the inspector presented the inspection results to Mr. S. Minahan, VicePresident-Nuclear and CNO, and members of his staff who acknowledged the findings. The inspector confirmed that no proprietary information was provided or examined during the inspection. | |||
AttachmentATTACHMENTSPersons ContactedJ. Bebb, Security ManagerT. Carson, Maintenance Manager R. Alexander, Electrical Superintendent M. Tackett, Outage Manager K. Billesbach, Quality Assurance Manager J. Larson, Quality Assurance Supervisor G. Griffith, Reactor Engineer Manager D.L. Willis, Operations Manager V. Bhardwaj, Engineering Support Manager D. Parker, Assistant Maintenance Manager D. Werner, Operations Training Supervisor R.A. Rexroad, System Engineer M. Metzger, System Engineer P.V. Fleming, Nuclear Safety Assurance Director G. Kline, Engineering Director T. Donovan, MP&C Manager R. Estrada, Corrective Action Program Manager M. McCormack, Electrical Systems/I & C System Engineering Supervisor M. Colomb, Plant Operations General Manager B. Kirkpatrick, Licensing Specialist D. Van Der Kamp, Licensing Manager J. Flaherty, Senior Staff Licensing Engineer S. B. Minahan, Site Vice President T. Hottovy, Equipment Reliability Manager D. Montgomery, Assistant to General Manager Plant OperationsDocuments ReviewedProcedure 0.5 Root Cause, Revision 5Administrative Procedure 0.5, "Conduct of the Condition Report Process," Revision 59 Administrative Procedure 0.5, "Condition Report Initiation, Review, and Classification," Revision 8 Administrative Procedure 0.5, "Condition Report Initiation, Review, and Classification," Revision 9 System Operating Procedure 2.2.20.2, "Operation of Diesel Generators From Diesel Generator Rooms," Revision 39 Human Performance High Intensity Training for Maintenance Personnel, Revision 02 Administrative Procedure 0-QA-09, "Supplier Evaluation Process," Revision 22 and 23 Maintenance Procedure 7.3.8.2, "Diesel Generator Electrical Examination and Maintenance," | AttachmentATTACHMENTSPersons ContactedJ. Bebb, Security ManagerT. Carson, Maintenance Manager R. Alexander, Electrical Superintendent M. Tackett, Outage Manager K. Billesbach, Quality Assurance Manager J. Larson, Quality Assurance Supervisor G. Griffith, Reactor Engineer Manager D.L. Willis, Operations Manager V. Bhardwaj, Engineering Support Manager D. Parker, Assistant Maintenance Manager D. Werner, Operations Training Supervisor R.A. Rexroad, System Engineer M. Metzger, System Engineer P.V. Fleming, Nuclear Safety Assurance Director G. Kline, Engineering Director T. Donovan, MP&C Manager R. Estrada, Corrective Action Program Manager M. McCormack, Electrical Systems/I & C System Engineering Supervisor M. Colomb, Plant Operations General Manager B. Kirkpatrick, Licensing Specialist D. Van Der Kamp, Licensing Manager J. Flaherty, Senior Staff Licensing Engineer S. B. Minahan, Site Vice President T. Hottovy, Equipment Reliability Manager D. Montgomery, Assistant to General Manager Plant OperationsDocuments ReviewedProcedure 0.5 Root Cause, Revision 5Administrative Procedure 0.5, "Conduct of the Condition Report Process," Revision 59 Administrative Procedure 0.5, "Condition Report Initiation, Review, and Classification," Revision 8 Administrative Procedure 0.5, "Condition Report Initiation, Review, and Classification," Revision 9 System Operating Procedure 2.2.20.2, "Operation of Diesel Generators From Diesel Generator Rooms," Revision 39 Human Performance High Intensity Training for Maintenance Personnel, Revision 02 Administrative Procedure 0-QA-09, "Supplier Evaluation Process," Revision 22 and 23 Maintenance Procedure 7.3.8.2, "Diesel Generator Electrical Examination and Maintenance," | ||
Revision 20Root Cause Investigation: CR 2004-7947 DG1 Inoperable Due to Lube Oil Fitting LeakRoot Cause Investigation: CR 2005-01360 DG1 Control Power Failure and Loss of Shutdown Cooling During Sequential Load Test Root Cause Investigation: CR 2007-00480 Unexpected Trip of Emergency Diesel Generator #2 During Surveillance Testing on January 18, 2007 Attachment-2-Root Cause Evaluation of the NRC White Performance Indicator for MSPI for EAC Exceeding theThreshold for EDG Run Demand Failures, CR-CNS-2007-01559, Revision 1Condition Report CR-CNS-2007-05645, Gap Analysis used to evaluate the finding in the Noticeof Violation against the original root causes in CR-CNS-2007-0480 and CR-CNS-2007-1559Condition Report CR-CNS-2007-07978Condition Report CR-CNS-2007-00058 Condition Report CR-CNS-2007-05140 Condition Report CR-CNS-2007-00114 Condition Report CR-CNS-2007-00623 Condition Report CR-CNS-2007-00898Emergency Diesel Generator Reliability Improvement Plan, Revision 4Diesel Generator Maintenance Improvement Team Plan Cooper Nuclear Station Equipment Trend Report, April-October 2007 Cooper Nuclear Station Monthly CAP Trend Report, October 2007 | Revision 20Root Cause Investigation: CR 2004-7947 DG1 Inoperable Due to Lube Oil Fitting LeakRoot Cause Investigation: CR 2005-01360 DG1 Control Power Failure and Loss of Shutdown Cooling During Sequential Load Test Root Cause Investigation: CR 2007-00480 Unexpected Trip of Emergency Diesel Generator #2 During Surveillance Testing on January 18, 2007 Attachment-2-Root Cause Evaluation of the NRC White Performance Indicator for MSPI for EAC Exceeding theThreshold for EDG Run Demand Failures, CR-CNS-2007-01559, Revision 1Condition Report CR-CNS-2007-05645, Gap Analysis used to evaluate the finding in the Noticeof Violation against the original root causes in CR-CNS-2007-0480 and CR-CNS-2007-1559Condition Report CR-CNS-2007-07978Condition Report CR-CNS-2007-00058 Condition Report CR-CNS-2007-05140 Condition Report CR-CNS-2007-00114 Condition Report CR-CNS-2007-00623 Condition Report CR-CNS-2007-00898Emergency Diesel Generator Reliability Improvement Plan, Revision 4Diesel Generator Maintenance Improvement Team Plan Cooper Nuclear Station Equipment Trend Report, April-October 2007 Cooper Nuclear Station Monthly CAP Trend Report, October 2007 | ||
}} | }} | ||
Revision as of 04:33, 31 August 2018
| ML080080622 | |
| Person / Time | |
|---|---|
| Site: | Cooper |
| Issue date: | 01/08/2008 |
| From: | Hay M C NRC/RGN-IV/DRP/RPB-C |
| To: | Minahan S B Nebraska Public Power District (NPPD) |
| References | |
| IR-07-010 | |
| Download: ML080080622 (16) | |
Text
January 8, 2008
Stewart B. Minahan, Vice President-Nuclear and CNO Nebraska Public Power District 77676 648A Avenue Brownville, NE 68321
SUBJECT: COOPER NUCLEAR STATION - NRC SUPPLEMENTAL INSPECTIONREPORT 05000298/2007010
Dear Mr. Minahan:
On December 6, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed aninspection at your Cooper Nuclear Station. The enclosed inspection report documents the inspection findings which were discussed on December 6, 2007, with you, and other members of your staff.The inspections examined activities conducted under your license as they relate to safety andcompliance with the Commission's rules and regulations and with the conditions of your license.
The inspector reviewed selected procedures and records, observed activities, and interviewed personnel. Based on the results of this inspection, no findings of significance were identified.
In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and itsenclosure will be available electronically for public inspection in the NRC Public DocumentRoom or from the Publicly Available Records (PARS) component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.gov/reading-rm/adams.html (the Public Electronic Reading Room).
Sincerely,/RA/Michael C. Hay, ChiefProject Branch C Division of Reactor ProjectsDocket: 50-298License: DPR-46
Enclosures:
NRC Inspection Report 05000298/2007010 Nebraska Public Power District- 2 -cc: w/enclosures:Gene Mace Nuclear Asset Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321John C. McClure, Vice President and General Counsel Nebraska Public Power District P.O. Box 499 Columbus, NE 68602-0499David Van Der Kamp Licensing Manager Nebraska Public Power District P.O. Box 98 Brownville, NE 68321Michael J. Linder, DirectorNebraska Department of Environmental Quality P.O. Box 98922 Lincoln, NE 68509-8922ChairmanNemaha County Board of Commissioners Nemaha County Courthouse 1824 N Street Auburn, NE 68305Julia Schmitt, ManagerRadiation Control Program Nebraska Health & Human Services Dept. of Regulation & Licensing Division of Public Health Assurance 301 Centennial Mall, South P.O. Box 95007 Lincoln, NE 68509-5007H. Floyd GilzowDeputy Director for Policy Missouri Department of Natural Resources P. O. Box 176 Jefferson City, MO 65102-0176 Nebraska Public Power District- 3 -Director, Missouri State Emergency Management Agency P.O. Box 116 Jefferson City, MO 65102-0116Chief, Radiation and Asbestos Control Section Kansas Department of Health and Environment Bureau of Air and Radiation 1000 SW Jackson, Suite 310 Topeka, KS 66612-1366Melanie Rasmussen, State Liaison Officer/ Radiation Control Program Director Bureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5th Floor 321 East 12th Street Des Moines, IA 50319John F. McCann, Director, LicensingEntergy Nuclear Northeast Entergy Nuclear Operations, Inc.
440 Hamilton Avenue White Plains, NY 10601-1813Keith G. Henke, PlannerDivision of Community and Public Health Office of Emergency Coordination 930 Wildwood, P.O. Box 570 Jefferson City, MO 65102Paul V. Fleming, Director of Nuclear Safety Assurance Nebraska Public Power District P.O. Box 98 Brownville, NE 68321Ronald L. McCabe, ChiefTechnological Hazards Branch National Preparedness Division DHS/FEMA 9221 Ward Parkway Suite 300 Kansas City, MO 64114-3372 Nebraska Public Power District- 4 -Daniel K. McGhee, State Liaison OfficerBureau of Radiological Health Iowa Department of Public Health Lucas State Office Building, 5 th Floor321 East 12 th StreetDes Moines, IA 50319Ronald D. Asche, President and Chief Executive Officer Nebraska Public Power District
1414 15 th StreetColumbus, NE 68601 Nebraska Public Power District- 5 -Electronic distribution by RIV:Regional Administrator (EEC)DRP Director (DDC)DRS Director (RJC1)Senior Resident Inspector (NHT)Branch Chief, DRP/C (MCH2)Senior Project Engineer, DRP/C (WCW)Team Leader, DRP/TSS (CJP)RITS Coordinator (MSH3)DRS STA (DAP)D. Pelton, OEDO RIV Coordinator (DLP)ROPreports CNS Site Secretary (SEF1)SUNSI Review Completed: __WCW____ADAMS: Yes G No Initials: _WCW Publicly Available G Non-Publicly Available G Sensitive Non-SensitiveR:\_REACTORS\CNS\2007\CNS95001IR.wpdRIV:SPE/CC:DRP/CWCWalkerMCHay/RA//RA/12/13/071/8/08OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax EnclosureU.S. NUCLEAR REGULATORY COMMISSION REGION IV Docket:50-298License:DPR-46 Report:05000298/2007010 Licensee:Nebraska Public Power District Facility:Cooper Nuclear Station Location:Brownville, Nebraska Dates:December 3 through December 6, 2007 Inspector:W. C. Walker, Senior Project Engineer, Branch C, Division of ReactorProjects (DRP)Approved By:M. C. Hay, Chief, Project Branch C, DRP ATTACHMENT:Supplemental Information Enclosure-2-SUMMARY OF FINDINGSIR05000298/2007010; 12/03/2007 - 12/06/2007; Cooper Nuclear Station. Inspection Procedure95001 Supplemental Inspection.The report covered a one-week period of inspection by a region-based inspector. No violationswere identified. The NRC's program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.Cornerstone: Mitigating Systems The U.S. Nuclear Regulatory Commission performed this supplemental inspection to assessthe licensee's evaluations of emergency diesel generator equipment problems associated witha performance indicator (Emergency AC Power) that crossed the Green-White threshold in the first quarter of 2007 and a related White finding involving inadequate corrective actions documented in NRC Inspection Report 05000298/2007007(ADAMS ML072290167). During this supplemental inspection, performed in accordance with Inspection Procedure 95001, the inspector determined that the licensee performed comprehensive evaluations of the three diesel generator failures that occurred since 2004. Specifically, the following three events contributed to the White performance indicator: 1) a lube oil sensing line leak in 2004 causing a failure of the diesel to run, 2) a control power failure in 2005 causing a diesel failure to start, and 3) a faulty voltage regulator circuit board in 2007 causing a diesel failure to run. On the basis of the licensee's evaluations for the above events the inspector determined that the primary root causes and corrective actions for the above performance issues were appropriately evaluated and implemented. In addition to the above issues a White finding was also identified for the January 2007 dieselfailure involving inadequate corrective actions related to repeat failures of the diesel generator voltage regulator circuit board. The licensee identified that the procedure for elevating repeat occurrences of problems to a root cause evaluation was inadequate. This deficiency resulted in the licensee's failure to perform a root cause evaluation following repetitive problems experienced with the emergency diesel generator voltage regulator circuit board following its installation. The root cause of the January 2007 event was determined to be: 1) a manufacturing defect of a zener diode on the voltage regulator circuit board, and 2) the process for maintaining quality of replacement safety-related components did not include the evaluation of operating experience for vendors removed from the approved suppliers list. Corrective actions to address the White finding included: 1) new procedures requiring burn in of electrical components were instituted, 2) a comprehensive review of all safety-related parts in the warehouse was conducted with holds placed on any parts that required further evaluation, and 3) the condition report procedure for escalation of repeat issues in the corrective action program was revised.Given the licensee's acceptable performance in addressing the diesel failures, the white findingassociated with this issue will only be considered in assessing plant performance for a total of four quarters in accordance with the guidance in Inspection Manual Chapter (IMC) 0305,
"Operating Reactor Assessment Program." Since the White finding was documented in the second calendar year quarter of 2007 the finding will remain in effect until the end of the first calendar year quarter of 2008.
Enclosure-3-Report Details 01INSPECTION SCOPEThe U.S. Nuclear Regulatory Commission performed this supplemental inspection toassess the licensee's evaluation associated with a performance indicator (Emergency AC Power) that crossed the Green-White threshold in the first quarter of 2007. The primary reason for this performance indicator being characterized as White was a second run failure of the emergency diesel generators in a 36 month period, on January 18, 2007. Overall, the Mitigating Systems Performance Index (MSPI) for the Emergency AC Power function represents three actual failures of the emergency diesel generators. This performance results in a change in core damage frequency that is characterized by industry standards as risk significant. An MSPI value of 5.7E-06/year was calculated for the three failures which exceeded the risk significance threshold of 3.4E-06/year as established by the industry and NRC. The change in core damage frequency resulting from the three failures represented by the emergency AC power MSPI value is characterized by the Reactor Oversight Process as a performance level that crosses the Green-White threshold. In addition to the White performance indicator the NRC staff also identified a Whitefinding and determined a corrective action violation occurred. The licensee failed to promptly identify a significant condition adverse to quality that resulted in reduced reliability of emergency diesel generator (EDG) 2. Two distinct and reasonable opportunities to identify the condition adverse to quality existed yet the condition was not promptly identified and corrected to preclude recurrence. Specifically, inadequate procedural guidance for evaluating the suitability of parts used in safety related applications presented one missed opportunity to identify that an EDG voltage regulating circuit board was defective prior to installation on November 8, 2006.
Following installation of the defective EDG 2 voltage regulator circuit board two high voltage conditions, one resulting in an EDG automatic high voltage trip, occurred on November 13, 2006. The licensee's evaluation of these high voltage events missed another opportunity to identify and correct the deficient condition. The failure to identify and correct this deficient condition resulted in an additional high voltage trip of EDG 2 that occurred on January 18, 2007. During this supplemental inspection, performed in accordance with InspectionProcedure 95001, the inspector determined that the licensee adequately determined the root causes and significant contributing causes of the Mitigating Systems Performance Index for Emergency AC Power crossing the Green-White threshold and the White finding for inadequate corrective actions, and established appropriate corrective actions to prevent recurrence.
Enclosure-4-02EVALUATION OF INSPECTION REQUIREMENTS02.01Problem Identificationa.Determination of who (i.e., licensee, self-revealing, or NRC) identified the issue andunder what conditionsThis supplemental inspection focused on two diesel failures to run which took place onDecember 30, 2004, and January 18, 2007. The initial failure resulted from installing a diesel lube oil sensing line different than specified in design documents, making the sensing line fitting susceptible to vibration induced high cycle fatigue. The second failure was due to a manufacturing defect of a zener diode in the voltage regulator circuit. Both of the failures to run of the diesel were self-revealing. In addition the January 18, 2007, issue was NRC identified as a White finding for inadequate corrective actions due to a failure to promptly identify a significant condition adverse to quality that resulted in reduced reliability of EDG 2.b.Determination of how long the issue existed and prior opportunities for identificationThe December 2004 diesel run failure involved a leak on the lube oil sensing line whichwas caused by the configuration of the sensing line components being different than specified in design documents, making the fitting susceptible to vibration-induced high cycle fatigue. The design change, which was implemented in May 1989 to prevent recurring tubing failures, was improperly performed. The December 30, 2004, failure was the fourth time since 1989 that this particular fitting had required repair. The root cause team determined that a contributing cause to the December 2004 event was a failure to identify and correct the design installation error during response to previous events. Prior identification was possible on the basis of three previous maintenance activities provided opportunities to discover and correct the configuration error. The details associated with this performance deficiency are documented in NRC Inspection Report 05000298/2005005 (ADAMS ML060450109).The January 2007 event involved a failure of the diesel to run due to a manufacturing defect of a zener diode on a voltage regulator circuit board. The board was purchased as a spare from the original equipment manufacturer in late 1973 prior to initial plant startup. The voltage regulator board remained in Nebraska Public Power District's inventory until installed in November of 2006 after a potentiometer on the EDG 2 voltage regulator board was damaged. The voltage regulator board that failed on January 18, 2007, was the replacement for the voltage regulator board whose potentiometer was damaged on November 8, 2006. After installation of the 33 year old voltage regulator board CR-CNS-2006-08999 documents that an over-voltage event within the EDG 2 voltage circuit control system occurred. The licensee concluded that the high voltage trip occurred due to erratic potentiometer operation during the tuning process for the voltage regulator circuit board. However, laboratory testing of the voltage regulator circuit board zener diode provided definitive evidence that the overvoltage trip of EDG2 was caused by an intermittent discontinuity in a diode resulting from a manufacturing defect. On the basis of further review the NRC identified that the Basler (voltage regulator vendor) technical manual for voltage regulators and the Electrical Power Research Institute both recommended replacement of the voltage regulator card Enclosure-5-following uncontrollable high voltage conditions. Voltage control problems on EDG 2had been addressed using apparent cause evaluations on four separate occasions in the twelve months prior to the November 13, 2006, high voltage trip. The November 13 trip was again assigned an apparent cause evaluation versus a more thorough root cause evaluation. The licensee's root cause assessment indicated that prior identification was possible if a more thorough evaluation was performed.c.Determination of the plant-specific risk consequences (as applicable) and complianceconcerns associated with the issueThe White Mitigating Systems Performance Index (MSPI) for the Emergency AC Powerfunction represents three actual failures of the emergency diesel generators. This performance results in a change in core damage frequency that is characterized byindustry standards as risk significant. An MSPI value of 5.7E-06/year was calculated forthe three failures which exceeded the risk significance threshold of 3.4E-06/year asestablished by the industry and NRC. The change in core damage frequency resulting from the three failures represented by the emergency AC power MSPI value is characterized by the Reactor Oversight Process as a performance level that crosses the Green-White threshold. In addition to the performance indicator turning White for the above events the NRCperformed a Special Inspection to review the circumstances surrounding the January 18, 2007, diesel failure. The results were documented in NRC Inspection Report 05000298/2007007 (ADAMS ML071430289). The NRC concluded that the best characterization of risk for the January 18, 2007, diesel failure was of low to moderate safety significance (White), with a delta CDF of 1.2E-6.02.02Root Cause and Extent of Condition Evaluationa.Evaluation of methods used to identify root cause(s) and contributing cause(s)To evaluate these three emergency AC power failure events, the licensee utilized thefollowing root cause analysis techniques:Problem Recognition and Interim ManagementInvestigation and Analysis Planning Cause Analysis and Determination Corrective Action Development and Assignment Corrective Action Implementation Effectiveness Measurement and FeedbackThe guidance for the use of cause determination techniques is contained inAdministrative Procedure 0.5 Root-Cause, "Root Cause Analysis Procedure," Revision 5. This procedure describes the six phases of the root cause analysis process, identifies important roles and responsibilities for the conduct of root cause analysis, and clearly delineates specific requirements to be adhered to during conduct of root cause analysis.
Enclosure-6-The inspector discussed the root cause determination process with the corrective action and assessment program manager. There are five individuals on site that are considered qualified to perform root cause analysis determinations. The qualification requirements for these individuals consists of formal classroom training, maintaining yearly qualifications, and actively participating in root cause determinations under the instruction of a qualified analyst. The inspector considered the licensee's root cause determination program to be appropriate.The inspector concluded that the quality of the root cause evaluations provided the rigorto ensure that the root cause evaluations were appropriate to determine the root causes and significant contributing causes of the diesel failures. b.Level of detail of the root cause evaluationThe licensee's root cause evaluations were thorough and identified the primary rootcauses of the performance issues. Specifically, for the December 30, 2004, event the configuration of the lube oil sensing line components were different than specified in design documents, making the swagelok fitting susceptible to vibration-induced high cycle fatigue. If the design change 89-022 had been properly followed the failure would not have occurred. The February 7, 2005, emergency diesel generator failure to start was a small contributor to the overall White performance indicator. It should be noted that the diode failure was a shorted diode as a result of an electrical overstress.
Regarding the January 18, 2007, diesel failure to run, a manufacturing defect in a zener diode on the voltage regulator control board was identified as the primary root cause for the failure.The root cause for the White finding involving the failure to promptly identify a significantcondition adverse to quality that resulted in reduced reliability of EDG 2 had two components. The first component was classification of a previous diesel failure in November 2006 as requiring less than a root cause evaluation even though it was a repeat occurrence. The second component involved the process for maintaining quality of replacement safety-related components did not include the evaluation of operating experience for vendors removed from the approved suppliers list. c.Consideration of prior occurrences of the problem and knowledge of prior operatingexperienceThe licensee's evaluations included a review of internal (Cooper Nuclear Station) andexternal operating experience. In general, these sections included relevant operating experience along with a discussion of how this applies or does not apply to the specific situation. d.Consideration of potential common cause(s) and extent of condition of the problemThe licensee's evaluation considered the potential for common cause and extent ofcondition for the failure to properly implement the design change for the lube oil sensing line on the EDG, the manufacturing defects in the voltage regulator circuit boards for the EDGs, and the control of safety related parts in the warehouse. The licensee's review of potential common causes for the lube oil sensing line leak determined that the most Enclosure-7-direct causal factor for the failure was vibration and that the tubing was configureddifferently than specified in the approved design change. The inspector determined that the licensee's extent of condition review was appropriate and thorough. The licensee performed a review of maintenance history and did not identify any concerns with other safety related systems. For the January 18, 2007, event it was determined that a random failure directly related to a manufacturing defect in the zener diode occurred.
The inspectors agreed with the licensee's assessment and determined that extensive testing was required to detect the manufacturing defect in the zener diode. The inspector concluded that the above actions combined with the corrective actionprogram changes appropriately addressed the weaknesses identified in the root cause reports. 02.03Corrective Actionsa.Appropriateness of corrective action(s)The specified corrective actions were appropriate to the root and contributing causesthat were identified in the root cause determination evaluations. As stated above, the root cause determinations were adequate to capture all aspects of the problems leading to the events. As a result, the specified corrective actions appeared to have addressed all possible causes and contributing causes. The licensee did identify in their root causeevaluations performed in response to the White performance indicator that prior opportunities existed to perform corrective actions which would have prevented the lube oil sensing line leak and would have potentially identified the defective voltage regulator circuit boards. The inspector agreed with this assessment and concluded that the lube oil sensing line leak was preventable had effective corrective actions been established following discovery of oil leaks at the Swagelok fitting location on four previous occasions between January 1993 and June 1999. The inspector noted that the corrective actions identified for the December 30, 2004, event addressed the design change/configuration control issues that ensured proper installation of the lube oil sensing tubing and reviewed other aspects of tubing configuration throughout the plant that would be effective in preventing recurrence.Regarding the January 18, 2007, EDG failure to run, resulting from a defective zener diode on a voltage regulator circuit board, a corrective action was identified that may have increased the likelihood that the defective zener diode would have been identified.
Specifically, testing of the voltage regulator circuit board using a burn-in or equivalent testing may have identified the infant mortality failure prior to its occurrence.The inspector's review of the corrective actions for the White finding determined thatproviding additional procedural guidance for escalation of repeat issues in the corrective action process should ensure that the appropriate level of licensee oversight is provided to ensure that a necessary root cause is performed when required. Additionally, a comprehensive review of all safety-related parts in the warehouse was conducted with holds placed on any parts that required further evaluation.
Enclosure-8-b.Prioritization of corrective actionsThe inspector did not identify any specific methods utilized to prioritize the specifiedcorrective actions based on risk significance or regulatory compliance. However, no examples of inappropriate prioritization were noted. The inspector considered the prioritization of the established corrective actions to be consistent with risk consequences.c.Establishment of schedule for implementing and completing the corrective actionsThe licensee established adequate schedules for completion of the specified correctiveactions. As appropriate, some corrective actions were tied to scheduled equipment outages while others were more short term such as procedure revisions or training updates. The inspector did not identify any specific concerns with the scheduling orcompletion of established corrective actions. The inspector did note that the diesel generator improvement plan regarding long termreliability improvements for the emergency diesel generators was included as a corrective action to be tracked in condition report CR-CNS-2007-01559. The inspector considered this initiative to be appropriate and should assist the licensee in the stated goal of the improvement plan to increase EDG reliability, availability, and maintenance predictability.d.Establishment of quantitative or qualitative measures of success for determining theeffectiveness of the corrective actions to prevent recurrenceThe licensee implemented a maintenance procedure change to the diesel generatorelectrical examination and maintenance procedure. This change included increased tasks to verify terminal tightness on diesel electrical equipment and perform thermography as a diagnostic tool to identify potential electrical problems in the EDGs prior to failure. The inspector interviewed station personnel involved in this effort and determined that this change had been implemented and was in use. The maintenance procedure specified the method, success criteria, and timing of this action in specific terms. The inspector identified no concerns in this area.The licensee also established controls on all safety-related parts in the warehouse toensure any parts that were not supported by documentation that ensured the parts were approved under an approved supplier program were placed on hold. The inspector reviewed this program and considered it appropriate to ensure only qualified safety-
related parts would be placed in the plant.
03MANAGEMENT MEETINGSExit Meeting SummaryOn December 6, 2007, the inspector presented the inspection results to Mr. S. Minahan, VicePresident-Nuclear and CNO, and members of his staff who acknowledged the findings. The inspector confirmed that no proprietary information was provided or examined during the inspection.
AttachmentATTACHMENTSPersons ContactedJ. Bebb, Security ManagerT. Carson, Maintenance Manager R. Alexander, Electrical Superintendent M. Tackett, Outage Manager K. Billesbach, Quality Assurance Manager J. Larson, Quality Assurance Supervisor G. Griffith, Reactor Engineer Manager D.L. Willis, Operations Manager V. Bhardwaj, Engineering Support Manager D. Parker, Assistant Maintenance Manager D. Werner, Operations Training Supervisor R.A. Rexroad, System Engineer M. Metzger, System Engineer P.V. Fleming, Nuclear Safety Assurance Director G. Kline, Engineering Director T. Donovan, MP&C Manager R. Estrada, Corrective Action Program Manager M. McCormack, Electrical Systems/I & C System Engineering Supervisor M. Colomb, Plant Operations General Manager B. Kirkpatrick, Licensing Specialist D. Van Der Kamp, Licensing Manager J. Flaherty, Senior Staff Licensing Engineer S. B. Minahan, Site Vice President T. Hottovy, Equipment Reliability Manager D. Montgomery, Assistant to General Manager Plant OperationsDocuments ReviewedProcedure 0.5 Root Cause, Revision 5Administrative Procedure 0.5, "Conduct of the Condition Report Process," Revision 59 Administrative Procedure 0.5, "Condition Report Initiation, Review, and Classification," Revision 8 Administrative Procedure 0.5, "Condition Report Initiation, Review, and Classification," Revision 9 System Operating Procedure 2.2.20.2, "Operation of Diesel Generators From Diesel Generator Rooms," Revision 39 Human Performance High Intensity Training for Maintenance Personnel, Revision 02 Administrative Procedure 0-QA-09, "Supplier Evaluation Process," Revision 22 and 23 Maintenance Procedure 7.3.8.2, "Diesel Generator Electrical Examination and Maintenance,"
Revision 20Root Cause Investigation: CR 2004-7947 DG1 Inoperable Due to Lube Oil Fitting LeakRoot Cause Investigation: CR 2005-01360 DG1 Control Power Failure and Loss of Shutdown Cooling During Sequential Load Test Root Cause Investigation: CR 2007-00480 Unexpected Trip of Emergency Diesel Generator #2 During Surveillance Testing on January 18, 2007 Attachment-2-Root Cause Evaluation of the NRC White Performance Indicator for MSPI for EAC Exceeding theThreshold for EDG Run Demand Failures, CR-CNS-2007-01559, Revision 1Condition Report CR-CNS-2007-05645, Gap Analysis used to evaluate the finding in the Noticeof Violation against the original root causes in CR-CNS-2007-0480 and CR-CNS-2007-1559Condition Report CR-CNS-2007-07978Condition Report CR-CNS-2007-00058 Condition Report CR-CNS-2007-05140 Condition Report CR-CNS-2007-00114 Condition Report CR-CNS-2007-00623 Condition Report CR-CNS-2007-00898Emergency Diesel Generator Reliability Improvement Plan, Revision 4Diesel Generator Maintenance Improvement Team Plan Cooper Nuclear Station Equipment Trend Report, April-October 2007 Cooper Nuclear Station Monthly CAP Trend Report, October 2007