ML20156A065

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NRR E-mail Capture - Final RAIs for Surry U1 Fall 2019 Sgtir Application
ML20156A065
Person / Time
Site: Surry Dominion icon.png
Issue date: 06/04/2020
From: Vaughn Thomas
NRC/NRR/DORL/LPL2-1
To: Geoffrey Miller
Dominion Generation
References
Download: ML20156A065 (3)


Text

From:

Thomas, Vaughn Sent:

Thursday, June 4, 2020 9:06 AM To:

gary.d.miller@dominionenergy.com

Subject:

Final RAIs for Surry U1 Fall 2019 SGTIR Application Attachments:

Final RAIs for Surry U1 Fall 2019 SGTIR.docx

Gary, The attached file constitutes the staffs issuance of the final RAIs concerning the Surry Unit 1 Fall 2019 Steam Generator Tube Inspection Report. As discussed today, June 4, 2020, the licensee agreed to provide its responses to the staff RAIs within 30 days from June 8, 2020 (due July 7, 2020).

Thank you, Vaughn Thomas, Project Manager Plant Licensing Branch II-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Vaughn.Thomas@nrc.gov 301-415-5897

Hearing Identifier:

NRR_DRMA Email Number:

620 Mail Envelope Properties (MN2PR09MB598098066BECCE700D30D0A8F4890)

Subject:

Final RAIs for Surry U1 Fall 2019 SGTIR Application Sent Date:

6/4/2020 9:06:26 AM Received Date:

6/4/2020 9:06:00 AM From:

Thomas, Vaughn Created By:

Vaughn.Thomas@nrc.gov Recipients:

"gary.d.miller@dominionenergy.com" <gary.d.miller@dominionenergy.com>

Tracking Status: None Post Office:

MN2PR09MB5980.namprd09.prod.outlook.com Files Size Date & Time MESSAGE 564 6/4/2020 9:06:00 AM Final RAIs for Surry U1 Fall 2019 SGTIR.docx 33174 Options Priority:

Normal Return Notification:

No Reply Requested:

No Sensitivity:

Normal Expiration Date:

SURRY POWER STATION UNIT 1 REQUEST FOR ADDITIONAL INFORMATION FALL 2019 STEAM GENERATOR TUBE INSPECTION REPORT DOCKET NO. 50-280 By letter dated March 11, 2020 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML20087H009), Virginia Electric and Power Company (the licensee) submitted information summarizing the results of the fall 2019 steam generator tube inspections performed at Surry Power Station (Surry), Unit 1. These inspections were performed during refueling outage (RFO) 29. Technical Specification (TS) 6.6.A.3 requires that a report be submitted within 180 days after Tavg exceeds 200°F following completion of an inspection of the SGs performed in accordance with TS 6.4.Q, Steam Generator (SG) Program.

To complete its review of the inspection report, the U.S. Nuclear Regulatory Commission staff requests the following additional information:

1. Please clarify the sampling strategy for eddy current examination of features such as dents, dings, and bulges in the Surry Unit 1 SGs. Table 1, Inspection Method for Applicable Degradation Modes, of the inspection report lists the methods used for inspections, but the report does not identify how inspection methods were applied to some special interest features (for example, the selection criteria for examination of dents and dings with specialized probes).
2. With respect to the secondary-side inspections, please clarify for each SG whether foreign objects or loose parts were removed, and the number and type of objects removed.
3. Table 3, Surry 1 EOC29 Inspection Summary-Non-AVB Volumetric Degradation, of the inspection report, which lists non-antivibration bar volumetric degradation, includes an indication in tube Row 33 Column 17, which the staff did not find in previous inspection reports. Please clarify whether this is a legacy indication or a newly reported indication that may be a result of recent degradation. If there is evidence of recent degradation, please discuss if a loose part may still be present. The staff notes that nearby tubes have previously reported loose part indications but without evidence of a loose part remaining.