ML20141H958

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Insp Repts 50-327/97-06 & 50-328/97-06 on 970525-0705. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML20141H958
Person / Time
Site: Sequoyah  Tennessee Valley Authority icon.png
Issue date: 07/28/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20141H951 List:
References
50-327-97-06, 50-327-97-6, 50-328-97-06, 50-328-97-6, NUDOCS 9708040130
Download: ML20141H958 (70)


See also: IR 05000327/1997006

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U.S. NUCLEAR REGULATORY COMISSION

REGION II

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Docket Nos:

50 327, 50 328

License Nos:

DPR-77, DPR 79

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Report Nos:

50 327/97-06, 50 328/97 06

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Licensee:

Tennessee Valley Authority (TVA)

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Facility:

Sequoyah Nuclear Plant, Units 1 & 2

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Location:

Sequoyah Access Road

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Hamilton County, TN 37379

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Dates:

May 25 through July 5,1997

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Inspectors:

M. Shannon, Senior Resident Inspector

R. Starkey, Resident Inspector

D. Seymour, Resident Inspector

W. Bearden, Region II (RII) Reactor Inspector (Section

M4.2 - M4.3)

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E. Testa, RII Reactor Inspector (Section R1)

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P. Taylor, RII Project Engineer (Section 07.2

07.2)

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S. Sparks RII Project Engineer (Section 07.2

07.3)

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J. Starefos, Resident Inspector, Browns Ferry Nuclear

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Plant (Section 07.2

07.5)

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C. Smith, RII Senior Reactor Inspector (Section E2.3 -

E2.4)

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E. Girard, RII Reactor Inspector (Section E1)

T. Scarbrough, Senior Mechanical Engineer, Office of

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Nuclear Reactor Regulation (NRR), (Accompanying

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Personnel)

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M. Holbrook, INEEL (Accompanying Personnel)

Approved by:

M. Lesser, Chief

Reactor Projects Branch 6

Division of Reactor Projects

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Enclosure 2

9708040130 970728

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ADOCK 05000327

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EXECUTIVE SUMMARY

Sequoyah Nuclear Plant, Units 1 & 2

NRC Inspection Report 50 327/97-06, 50 328/97 06

This integrated inspection included aspects of licensee operations,

maintenance, engineering, plant support, and effectiveness of licensee

controls in identifying, resolving, and preventing problems. The report

covers a six week period of resident inspection.

In addition, it includes the

results of announced inspections in the areas of engineering, maintenance,

corrective action program, and health physics performed by regional and

headquarters inspectors.

Operations

Operations successfully performed significant power changes on Unit 2 to

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repair a failed letdown isolation valve, to repair a failed sensing line

on the 28 main feedweter pump, and due to a main transformer relay

actuation; and on Unit 1 to repair a main feedwater pump (Section 01.1).

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A non cited violation was identified for the failure of the licensee to

perform steps of a procedure in the correct sequence, resulting in

establishing a flow path for essential raw cooling water to enter and

contaminate the "A" condensate storage tank (Section 01.3).

A weakness in operator training was identified for the failure of two

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operator trainees to successfully parallel emergency diesel generators

to their shutdown boards (Section 05.1).

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A Quality Assurance outage assessment effort was substantial and was

effective in the identification of licensee strengths and weaknesses

during the Unit 1 Cycle 8 refueling outage (Section 07.1).

The implementation of the Corrective Action Program (CAP) processes

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appeared to have improved since the audit of October 1996. However, the

monthly CAP status reports, and weaknesses with Problem Evaluation

Reports (PER) identified during this inspection, indicated that

improvement may not be continuing. Continued management attention and

Nuclear Assurance involvement, along with more effective implementation

by the line organization of the CAP process is necessary.

(Section 07.2).

Self assessments by operations resulted in several improvement

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initiatives. The peer review program, in combination with review of

PERs and other related material, has been succes.sful in identifying the

raw data from which corrective actions can be developed and implemented.

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However, recent issues are evidence that actions in response to self-

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assessments have not resulted in sustained improvements in performance.

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(Section 07.3).

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A positive observation was noted for operation's timely identification

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of improper work activities on the excess letdown valve (Section M4.1).

Maintenance

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Self assessments by maintenance provided an accurate picture of the

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performance of the maintenance department. A declining trend in the

maintenance area was identified following a more thorough and critical

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review of self assessment and other site information. Corrective

actions to address the identified weaknesses have been developed, most

notably in the area of personnel accountability, human performance, and

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supervisory oversight.

However, recent issues are evidence that actions

in response to self-assessments have not yet been fully effective

(Section 07.3).

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During plant power changes, numerous equipment problems and material

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condition deficiencies caused challenges to the operations staff

(Section 01.2).

A positive observation was noted with the extensive troubleshooting plan

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and post maintenance testing plan developed by the maintenance manager

with the support of engineering (Section M1.2).

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The pre job briefing for the replacement of a Unit 2 Loop 2 steam

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generator level controller was thorough, and the replacement of the

controller by instrument maintenance personnel was carefully performed.

The entire evolution was well planned and executed (Section M1.3).

A non cited violation was identified for failure to inspect both sides

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of nine fire barrier penetrations (Section M1.4).

A positive observation was noted with housekeeping improvement in the

turbine building (Section M2.1).

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One non cited violation was identified for failure to follow maintenance

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instructions during repair work on a Unit 2 excess letdown isolation

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valve (Section M4.1).

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Significant corrective actions were taken, or were in the process of

being completed, for the deficiencies identified by the licensee in

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their May 5, 1997, Generic Letter (GL) 96 01 Report. A non cited

violation was identified for four examples of inadequate surveillance

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instructions related to the GL 96 01 review.

Required surveillance

testing was performed during the March 1997 refueling outage, and prior

to reactor startup following the forced outages in June 1996 and

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November 1996 (Section M4.2 and M4.3).

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Implementation of Generic Letter 89-10 at Sequoyah was not sufficiently

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complete to permit closure of the NRC review (Section E1.1).

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Weaknesses were identified in the analyses of stroke time failures of

turbine driven auxiliary feedwater trip and throttle valve 1-FCV 151

documented in two PERs (Section E1.1 and E2.2).

The licensee employed personnel who were knowledgeable of industry

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issues and obtained accurate diagnostic measurements in implementing

Generic Letter 89 10 (Section E1.1).

A violation was identified for the licensee's failure to implement

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adequate corrective actions to correct the improper setting of the

safety injection system relief valves. (Section E2.1).

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Corrective actions developed and implemented for motor cperated valves

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not having "T" drains in their limit switch compartments were consistent

with design requirements and NRC's guidance in Generic Letter 91-18

(Sectior.E2.3).

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The overall quality of plant modifications M8779A and M8780A was

determined to be good. The broad scope of the plant modifications have

achieved the design objective of re-establishing configuration control

for Sequoyah's Environmental Qualification Program (Section E2.4).

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Plant Sucoort

The inspectors determined that the licensee effectively implemented a

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program for shipping radioactive materials required by the Nuclear

Regulatory Commission and Department Of Transportatien regulations

(Section R1.2).

Radiological facility controls and housekeeping in radioactive waste

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storage areas were observed to be good. Material was labeled

appropriately, and areas were properly posted (Section R1.3).

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Radiation worker internal and external doses were being maintained well

below regulatory limits and the licensee was continuing to maintain

exposures as low as reasonably achievable (Section R1.3).

One non cited violation was identified for failure of a radiographer to

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follow site procedures (Section R1.3).

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A violation was identified for failure to replace the rubber gasket-

seals for railroad tracks required to maintain the auxiliary building at

a negative pressure as described by the Updated Final Safety Analysis

Report and detailed design documents (Section R1.3).

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The licensee's water chemistry control program for monitoring primary

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and secondary water quality had been implemented, for those parameters

reviewed, in accordance with the Technical Specification requirements

(Section R1.4).

The Fuel Integrity Assessment team was aerforming the required fuel

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integrity assessments as specified by tie Site Standard Practice

(Section R1.4).

The radiological impact from facility operation was less than 1 percent

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of the 40 CFR 190 regulatory limit. The exposures calculated from the

1996 Annual Radioactive Effluent Release Report resultant data were

consistent with results from the preoperational monitoring program

(Section R1.5).

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Report Details-

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Summary of Plant Status

a.

Unit 1 began the inspection period in power operation. The unit operated at

100% power until June 28,'when power was reduced to 62* for maintenance on the

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main feed pumps,

Power was restored to 100% on June 30, and the unit operated

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at power for the remainder of the inspection period.

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Unit-2 began the inspection period in power operation. The. unit operated at

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100% power until~ June 6 when power was reduced to approximately 28% to repair

the normal letdown isolation valve.

Power was restored to 100% on June 9 and

the unit operated at 100% power until June 18,:when power was reduced to

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approximately 56% to remove and re) air the 2B main feed pump. Power was

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restored to 100% on June 19, and t1e unit operated at 100% until July 4, when

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power was reduced to approximately 60% due to a main transformer Bucholtz

relay actuation (high combustible gas concentration).

Power was restored to

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100% on July 5, and operated at 100% for the remainder of the inspection

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period.

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Review of Vodated Final Safety Analysis Reoort (UFSAR) Commitments

While performing inspections discussed-in this report, the inspectors reviewed

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the applicable portions of the UFSAR that were related to the areas inspected.

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The inspectors verified that the UFSAR wording was consistent with the

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observed plant practices, procedures, and/or parameters.

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I. Qge_ rations

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Conduct of Operations (71707)

01.1 General Comments-

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Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations.

In general, the conduct of

o)erations was good. Operations successfully made significant power

clanges on Unit 2 to repair a failed letdown isolation valve, to repair

a failed sensing line on the 2B main feedwater pump, and due to a main

transformer relay actuation; and on Unit 1 to repair a main feedwater

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pump. Specific events and noteworthy observations are detailed in the

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sections below,

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01.2 Operational Challenaes Durina Plant Power Chanaes

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a.

Inspection Scope

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The' inspectors reviewed the various operational challenges encountered

during the four significant unit power reductions to perform plant

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repairs.

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b.

Observation and Findinas

The inspectors noted various equipment problems that were being

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encountered during plant power changes. The equipment problems varied

during each plant transient: however, the problems were unexpected and

resulted in operational challenges. The inspectors observed some of the

failures and noted the other failures in the control room logs. The

failures were as follows:

Unit 2 Power Reduction to 28% on June 6, and Power Increase to 100% on

June 9.

During the initial load decrease:

a feedwater regulating valve caused a

7% level deviation; the letdown heat-excharger outlet flow indicator

failed: when removing the #3 heater drain tank pump, the #3 heater drain

tank level started oscillating, resulting in LCV 6 105A opening and

closing repeatedly: fire protection to the seal oil unit was isolated

due to a failure of 2 FCV 26 72 to reset; the pressurizer spray line

temperature " low temperature" alarm annunciated, causing the operators

to take manual control of the pressurizer spray valve: while removir.g

the 2A main feedwater pump from service: the governor valve positioner

stopped moving and appeared to be stuck: the Neutral Overcurrent relay

for the "B" cooling tower transformer picked up. causing the "B" common

station service transformer sup)1y breaker to trip and actuation of the

fire protection system: the hig1 pressure gland steam pressure began

oscillating and bringing in computer alarms; and the excess letdown

valve failed closed.

(Refer to Section M4.1).

During the power increase:

operators had difficulty adjusting the #3

heater drain tank level due to the heater drain tank pump recirc valve

leaking through; the main steam reheat warming valves were found closed

when they should have been opened per 0-G0 4, Step (16); and operators

received a " Computer Alarm Rod Deviation and Power Range Tilts" alarm

due to a high upper detector quadrant power tilt ratio.

Unit 2 Power Reduction to 56% on June 18 and Power Increase to 100% on

June 19.

During the power decrease: operators received the pressurizer spray

line temperature low alarm: operators received a ground alarm on the 250

V DC battery due to a 160 volt ground; the "A" main feedwater pump did

not load up as cuickly as expected, resulting in operators reducing

turbine load anc taking manual control of the feedwater regulating valve

to dampen the level swings and the #2 steam generator level was slower

to recover than the other levels; and the axial flux difference (AFD)

went out of the administrative target band.

During the power increase: the 2B condensate booster pump developed

excessive seal leakage: and the 2C condensate booster pump recirc valve

developed significant leakage.

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Unit 1 Power Reduction to 62% on June 28 and Power Increase to 100% on

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June 30.

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During the power decrease:

the C-4 heater level went low and the normal

level control valve was found stuck: the 18 B main feedwater pump

' suddenly unicaded almost 1 million pounds mass per hour, the 1A A main

feedwater pump _apwared to have overcompensated and feedwater pressure

went too high; a )roblem Evaluation Report (PER) was initiated for

decreasing power (17% per hour) in excess of the planned 10% per hour:-

the 1A A main feedwater pump had to be taken to manual to settle out

steam generator flow swings: and the main transformer phase "A" group #1

fan #10 appeared to be locked up.

Ouring the power increase: the "B" condensate booster pump was already

warmed up due to the suction valve leaking through; and the "A" air

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compressor tripped on high oil temperature,

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Unit 2 Power Reduction to 60% on July 4 and Power Increase to 100% on

July 5.

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During the power increase: the 2A condensate booster pump tripped

during the start sequence due to an excessive amount of water in the

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pump's oil system; and the AFD monitor alarm was suspected of being

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inoperable due to the AFD being outside the target band and with no

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alarm reflash capability.

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The problems, while not all inclusive indicated a need for further

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licensee effort in improving plant equipment reliability. They also

appeared to present a high number of challenges to the operations staff,

mtentially causing the operators to see these challenges as routine.

Related to this, is a Nuclear Assurance finding (weakness) detailed in-

Section 07.1 of this, report that stated, "When abnormal and/or

unanticipated actions occurred, control room personnel generally reacted

to the conditions as a normal evolution, when a more appropriate

response would be to stop and establish a clear understanding of the

condition."

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Conclusions

Each equipment failure, by itself, did not present a safety significant

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problem however, the collective number of failures during each evolution

challenged the operators and indicates material condition weaknesses.

01.3 Essential Raw Coolina Water (ERCW) Enters Condensate Storaae Tank

(CST) via Auxiliary Feedwater System (AFW)

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Insoection ScoDe

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The inspectors reviewed the circumstances which resulted in ERCW water

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(river water) entering the "A" CST via the AFW system.

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b.

Observation and Findinas

On April 29, 1997, with Unit 1 in Mode 5, during performance of

Surveillance Instruction (SI) 1-SI 0PS 003-118.0, Auxiliary Feedwater

Pump and Valve Automatic Actuation, Revision 3, the ERCW flow control

valves (FCV) to the turbine driven auxiliary feedwater (TDAFW) pump

opened unex>ectedly. The valves were o)en for approximately two minutes

during whic1 time a flow path existed w11ch allowed ERCW water to go to

the TDAFW pump suction, out the common recirculation line, and then to

the CSTs.

Prior to this occurrerce, the 1 SI 0PS 003 118.0 lineup had

isolated the steam generators to prevent flow from the AFW system. On

the following day, April 30, the chemistry laboratory re)orted that CST

"A" had elevated chloride levels.

It was at that time t1at the flow

path from the TDAFW was identified as the source of the elevated

chloride levels.

Prior to the performance of 1 SI 0PS-003-118.0 TDAFW CST suction valve

1-VLV 003-809 was tagged closed due to concern for excessive leakage out

of the pump outboard seal. The ERCW FCVs were already tagged closed as

required by General Operating procedure 0 G0-7 Unit Shutdown From Hot

Standby to Cold Shutdown. The TDAFW pump suction pressure switches for

Wap over to ERCW are located between the CST suction valve and the

pump. Due to the location of the pressure switches, with the CST

suction valve closed, the low suction pressure switches for the swap-

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over to ERCW were in the " actuate" position. This low pressure

condition caused the " low suction pressure to the AFWPs" alarm window to

be illuminated. However, the presence of this alarm was not addressed

in the pre job briefing, nor was it questioned by the operators or the

test director during the briefing. With the TDAFW low suction pressure

input present, only the TDAFW trip and throttle valve being greater than

50% open was needed, once power was restored, to cause the ERCW FCVs to

open.

In preparation for 1-SI 0PS-003 118.0, the Test Director released the

hold order on the ERCW FCVs to all three Unit 1 AFW pumps, which placed

power on all ERCW FCVs. The lifting of the hold order took place prior

to Section 6.1 of 1 SI 0PS-003118.0, but was not directed by the

procedure until Sections 6.5 and 6.7.

During aerformance of Section 6.2

of the SI, an actuation signal was initiated w11ch resulted in the TDAFW

trip and throttle valve opening. When the trip and throttle valve

opened, the logic was completed (low suction pressure from the CST and

trip and throttle valve being greater than 50% open) and the ERCW FCVs

opened.

Steps in Sections 6.5 and 6.7 would have prevented the FCVs

from opening if the hold order had been released in the correct

sequence. The test director, who was in the control room, noticed the

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ERCW valves going open. Operators promptly closed the valves. Actual

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open time was approximately two minutes from the TDAFW start signal to

closure of the valves by operators.

The inspector reviewed the licensee's corrective actions, as detailed in

PER No. SQ971275PER, and concluded that they were appropriate to prevent

recurrence of this event.

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The licensee failed to perform steps of procedure 1 SI 0PS-003118.0 in

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the correct sequence which resulted in establishing a flow path for ERCW

to enter and contaminate the "A" CST. This licensee identified and

corrected violation is being treated as a non cited violation (NCV),

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consistent with Section VII.B.1 of the NRC Enforcement Policy

(NCV 50 328/97 06 01).

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Observations

One NCV was identified for failure to follow procedure steps in

sequence.

05

Operator Training and Qualification

05.1 Emeroency Diesel Generator (EDG) Testina

a.

Inspection Scong

The inspectors reviewed the circumstances of two EDG output breakers

tripping open while paralleling the EDGs to their shutdown boards during

two consecutive weekly surveillance tests.

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Observations and Findinas

On June 6 and June 12, while performing 2 SI 0PS 082-007.A. Electrical

Power System Diesel Generator 2A A, and 2-SI 0PS-082 007.B. Electrical

Power System Diesel Generator 2B-B, the output breakers for the 2A-A and

2B B EDGs, respectively, tripped open while the EDGs were being

parallelled to their shutdown boards.

In each case, the generator

output breaker tripped on instantaneous overcurrent. On June 6 the

instantaneous overcurrent relay was reset and the diesel was

successfully synchronized to the shutdown board. On June 12. the

instantaneous relay was checked and reset, the generator tested, and the

EDG successfully rerun and synchronized to the shutdown board.

The licensee determined the cause of the output breakers tripping was

inexperience of the operators (trainees) in synchronizing the EDGs to

their shutdown boards. The 3rocedure requires the operator to adjust

the synchronizing scope to o)tain an indication of slowly rotating in

the fast direction, and to close the breaker when the synchroscope

indicates between the five minutes till and 12 o' clock position, which

the trainees did.

If the synchronizing scope is rotating too slowly in

the fast direction, and/or the breaker is closed at a slightly greater

than five minutes to 12 o' clock >osition, an overcurrent condition can

result, tripping the EDG output areaker. The licensee concluded that

the operator trainees were acting in an overly cautious manner by

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adjusting the synchronizing scope to travel too slowly in the fast

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direction, and by closing the breaker at that slow speed at five minutes

to the 12 o' clock position. The licensee implemented procedure change

forms to revise the procedures for both units to require closing the

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breaker when the indication is at 12 o' clock.

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c. ' Conclusions

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The inspectors considered the failure of the two operator trainees to

successfully parallel the EDGs to their shutdown boards to be weakness

in operator training.

07

Quality Assurance in Operations (40500)

07.1 Review of the Unit 1 Cycle 8 Quality Assurance (0A) Outaae Assessment

a.

Inspection Scope

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The inspector reviewed the Unit 1 Cycle 8 outage oversight assessment

(NA-SQ 97 43) to gain an independent review of licensee performance

during the refueling outage.

b.

Observations and Findinas

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The inspector noted that the Nuclear Assurance assessment team (13

members) initiated 125 PERs during the outage. The team reached the

following global conclusions which were documented in the assessment

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report, "The report identified numerous recurring human performance

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issues in the areas of conduct of operations, conduct of maintenance,

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and line verification due to procedure noncompliance and conflicting

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work standards. Overall, the self-assessment process appears to be less

than fully effective in monitoring / enforcing / correcting problems at the

first level of supervision."

The nuclear assurance team noted the following weaknesses:

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Apparent varying (conflicting) operations performance standards,

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and operators not performing daily and frequently performed tasks

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with the same accountability as sensitive work activities,

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Critical evolutions not recorded in operator logs, and log entries

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that were either inaccurate or insufficiently documented,

The conduct of event critiques needed improvement,

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Observation of the residual heat removal

xamp cavitation

[defueled] and reactor coolant system leac during restoration

indicated an area for improvement. When abnormal and/or

unanticipated actions occurred, control room personnel generally

reacted to the conditions as a normal evolution. A more

appropriate response would have been to stop and establish a clear

understanding of the condition,

The conduct of the Plant Operations Review Committee (PORC)

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continued to be a weakness: PORC scheduling and formality needed

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to improve,

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The plant's response to QA identified issues concerning the

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January adverse trend PER on procedural adherence, and the

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November PER on wrong unit / wrong train / wrong component was not

prompt and resulted in a missed opportunity to improve the areas

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prior to the outage.

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The nuclear assurance team noted the following strengths:

Overall planning and prioritization of outage activities were

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focused toward improvement of plant material conditions,

Positive management improvement initiatives were being

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implemented,

The conduct of complex and infrequently performed test pre-job

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briefings was good.

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Site engineering support improved significantly,

Improvement initiatives were implemented to capture lessons

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learned from Watts Bar and Browns Ferry,

The goals and objectives for improving plant material condition

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were fully accomplished,

The management oversight / observation process was expanded to

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include medium risks evolutions.

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The inspector noted that the assessment included extensive documentation

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of these findings. The inspector also noted that three of the weaknesses

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were related to and/or supported previously documented NRC inspection

report (IR) findings.

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c.

Conclusions

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The inspector concluded that the QA outage assessment effort was

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substantial and was effective in the identification of licensee

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strengths and weaknesses during the Unit 1 Cycle 8 refueling outage.

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07.2 Corrective Action Program

a.

Inspection ScoDe

Using the guidance of Inspection Procedure 40500. Effectiveness of

Licensee Controls in Identifying, Resolving, and Preventing Problems,

the inspector reviewed licensee's corrective action program (CAP) as

delineated in SSP 3.4, Corrective Actions. The review included an

evaluation of the quality of PERs, an assessment of Management Review

Committee (MRC) involvement in the CAP process and whether the CAP

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requirements are being effectively implemented.

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b.

Observations and Findinas

The inspector reviewed corporate NA&L audit report SSA 9509, dated

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July 31,1995. This audit identified significant weaknesses concerning

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the CAP implementation and PER No. SQ950563PER was issued to address the

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audit finds, which were:

Inadequate or incomplete root cause analysis.

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Some identified adverse conditions were not being documented in

the corrective action program as required.

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Examples of tardiness in the developing (20 working days) and

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implementing (60 working days) of PER corrective actions.

Examples of inadequate root cause determinations leading to high

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levels of recurrence.

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Examples of no interim actions being assigned to PERs, nor

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reviewed by management.

A subsequent NA&L audit of the CAP (SSA 9613 dated November 4, 1996)

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showed that the problems identified in SSA 9509 audit continued to

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occur. An NA&L Escalation Report was presented to site management on

October 17, 1996, to demonstrate that previous corrective actions had

not been thorough and that apparent cause analysis and extent of

condition did not probe dee ly enough, resulting in incomplete

resolution of CAP issues.

he licensee issued PER No. SQ962389PER to

address the SSA 96013 audit finding.

The inspector reviewed the implementation of corrective actions

associated with several PERs, including PER No. SQ962389PER, and also

observed MRC meetings. The following observations resulted from these

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reviews:

The site QA organization has initiated continuous oversight of the CAP

processes.

Indicators are established to monitor CAP implementation

with a status report being issued monthly. The status report identifies

problem areas which require management attention. The ins)ector's

assessment of the data from these monthly status reports (iovember 1996

May 1997) indicated that CAP implementation improvement is not

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continuing.

Repetitive issues that continue to appear in these status

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reports were:

tardiness in the development and implementation of PER

corrective actions: the quality of tP corrective action plans and the

PER closure packages: weak similar ever.. and extent of condition

searches; and improvement in the line organizations ability to identify

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deficiencies during their self assessments of the CAP process

implementation.

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The inspector reviewed some PERs written on the auxiliary feedwater

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system (AFW) and PER No. SQ962526PER, which identified that NA&L had not

established effective oversight of the CAP for an approximate 18 month

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period (April 1995 - September 1996).

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The inspector noted that Block 4 of PER No. SQ962526PER, "Immediate

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Actions Taken," had no assigned actions.

Block 9 of the PER,

" Corrective Action," had no specific corrective actions identified,

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except for a statement that an assessment of the site corrective action

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program implementation would be conducted in June 1997.

In discussing

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these concerns with QA personnel, the inspector determined that multiple

immediate actions and other corrective actions had been taken by the

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licensee, but had not been documented on the PER. Subsequently, PER No.

SQ962526PER was revised to reflect corrective actions taken and planned.

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The inspector noted that many PERs selected for review on the AFW system

had previously been evaluated by NA&L. NA&L had identified deficiencies

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with most of these PERs which were corrected. No additional

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deficiencies were identified.

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During a walkdown of the Unit 110AFW system it was noted that two steam

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traps in parallel drain piping were covered with insulation. The

-inspector questioned whether the insulation could affect the ability of

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the steam traps to perform their function.

During a subsequent

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walkdown, the ins)ector observed that insulators were removing the

insulation from t1e Unit 1 steam traps. The inspector brought to the

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licensee management's attention that a PER was not immediately

initiated, and subsequently PER No.

SQ971512PER was written. The PER

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indicated that an inspection of Unit 2 TDAFW system revealed that there

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was no insulation on the drain piping or steam traps, as per drawing

requirements, and that the Unit 1 drawings were not clear on insulation

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requirements.

In a subsequent telephone call with a Licensing

Department contact, the inspector was informed that the licensee had

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contacted the steam trap vendor and concluded that the steam trap will

still perform its function if insulated.

The licensee made changes (memorandum October 4, 1996, and April 28,

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1997) to MRC activities in order to strengthen line manager's ownership

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of the CAP process. Changes made included the deletion of the PER

Review Subcommittee functions and the establishment of requirements for

the HRC to review the corrective action plans for all Level A and B PERs

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as well as selected Level C PERs.

The inspector observed MRC meetings on June 3-6, 1997, and noted that

discussions were on PERs which were returned to the MRC for review of

proposed corrective actions. The PER evaluation summaries returned to

the MRC, in general, addressed a description of the condition, immediate

action taken, interim action, previous similar events, extent of

condition, apparent cause, and corrective action. The inspector noted

that the MRC did not accept all PER corrective action plans as presented

to the MRC. For example, PER No. SQ971036PER's corrective action plan,

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which was discussed at the HRC meeting on June 5, 1997, was returned to

the preparer to address aspects.

The MRC actions taken during the meetings appeared to be consistent with

their charter,

c.

Conclusion

The implementation of CAP processes appeared to have improved since the

audit (SSA 96013) of October 1996.

However, the monthly CAP status

reports, along with weaknesses with PERs identified during this

inspection, indicated that improvements in implementing the CAP

processes may not be continuing and has leveled off.

Continued

management attention along with more critical self assessment by the

line organization and more effective implementation of the CAP 3rocess

is necessary. This is of particular importance as the site NA&_ plans

to stop the continuous oversight of the CAP in the very near future.

07.3 Line Oroanization Self-Assessment

a.

Inspection Scope

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The licensee's self-assessment of operations was reviewed and evaluated,

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which included the program as described in Operations Directive Manual

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ODM 0.5, and the observation / peer checks of job and training performance

as described in ODM 0.6.

In addition, the licensee's self assessment of maintenance was reviewed

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and evaluated, which included a review of the Site Trend Analysis

Committee reports, quarterly maintenance and modifications self-

assessments, and the peer evaluation program and reports.

b.1 Observation and Findinas - Operations Self Assessment

The inspectors reviewed the following self assessment information, and

other data provided by the licensee:

The operation's self assessment program as described in ODM 0.5. The

program consists of analyzing trends using performance indicators. A

major source of data is provided by the Observations Sheets from ODH-

0.6, PERs, and a monthly activity report provided by NA&L.

ODM 0.6, Observationheer checks of job and training performance. This

program is based on lip 0 guidelines, and participation of the operations

department has been good. Current improvement initiatives included

sending operating crews to other plants to identify good operating

practices, continuing to stress improvement in plant material condition

such as operator work-arounds, main control room disabled functions, the

creation of a mentoring program by assigning a supervisor to each

operator, emphasis on procedural compliance, and pre job briefs. The

peer review pre-am has also resulted in the generation of many PERs.

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The most recent quarterly review, which w,

completed for the period

January 1 to March 31, 1997, and identifieu satisfactory or good

performance in all areas except fire arotection systems, which was

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identified as needing improvement. T1e inspector noted that performanca

in plant status controls had changed from "needing improvement" to

" satisfactory" since the previous quarter.

ODM 1.4, Operations Top Ten Concerns.

Some of the concerns included

establishing a "mentoring" program within operations crews, assistant

unit operator (AU0) watchstanding practices / visits at other sites,

operator work arounds, reduction of procedural adherence events by

operators, and inter / intra department communications.

Level B PER No. SQ970199PER, initiated by Industry Affairs in late

January 1997, due to an adverse trend in procedural compliance for the

period of July December 1996.

Minutes of a recent Nuclear Safety Review Board Operations Subcommittee

meeting, held in March 1997, where several opportunities for improvement

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were noted in the area of operations self-assessments. These included

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additional management observations of the AVO staff, training of the

shift management personnel in observation skills, and inclusion of

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cross discipline activities in the self assessment 3rogram. A concern

was expressed by operations shift management that t1e self-assessment

program focused too much on quantity and not quality. The inspector

discussed these observations with operations management, who indicated

that actions were being taken or developed to address these concerns.

The inspector agreed that a substantial quantity of data was being

generated as a result of the operations self assessments. This was due

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to the increase in the number of PERs from prior years, and the peer

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review program.

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'Recent problems and events associated with plant operations. These

problems include control room communications and oversight, control room

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logs, and corrective actions as discussed in NRC irs 50-327, 328/97 04

and 97 05.

In addition, recent NA&L assessments and/or PERs have also

identified continuing concerns in procedural compliance and status

control, and other human performance problems. These issues indicate

that operation's self asse: sments have not resulted in substantive

improvements in the operations area.

b.2 Observations and Findinas

Maintenance Self Assessment

The inspectors reviewed and discussed the peer evaluation program with

maintenance personnel.

For calendar year 1996, over 1500 peer

evaluations were conducted, with a similar number on schedule for 1997.

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This information is reviewed monthly for strengths or weaknesses, and

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the information is sent to the training center to review for potential

training issues. The inspector's review of the peer evaluation cards

indicated that substantive information and feedback was being

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identified. The inspectors consider the participation in the peer

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evaluation program by maintenance supervision to be good.

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Based on the peer evaluation program and NA&L monthly trends, the

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maintenance self assessment identified that performance had declined in

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several areas.

These areas included plant material condition, conduct

of maintenance, maintenance procedures and documentation.

In addition,

switchyard activities were noted as still needing improvement, and

maintenance history was identified as unsatisfactory.

Based on this

declining trend, maintenance concluded that the standards and

accountability of maintenance personnel at all levels needed to be

improved, and several corrective actions were taken. An outside

contractor was brought in to help ~ focus on supervisor and general

foreman performance, and each was re evaluated for their individual

performance. Supervisory training was conducted, and included the

development of a guideline book describing management expectations.

Performance criteria for each supervisor was re written to reinforce

performance expectations. Scenario training was used to reinforce and

coach administrative and procedure adherence skills with craft

personnel. The threshold for technical training grade level acceptance

was changed from 70% to 80%.

The inspectors also reviewed a site wide common cause assessment,

conducted in March 1997. This effort reviewed data from the last six

months of 1996, and was the third such assessment-to be conducted by the

site. The assessment noted that corrective actions were already in

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place to improve problems associated with attention to detail,

inadequate job skill and work practices, and these efforts were

partially effective. However, as discussed earlier, a Level A PER No.

SQ971488PER was initiated June 2, 1997, by NA&L due to an adverse trend

identified for human performance during the Unit 1 Cycle 8 refueling

outage for conduct of maintenance and operations.

c.

Conclusions

Self assessments by operations resulted in several improvement

initiatives. The peer review program, in combination with review of

PERs and other related material, has been successful at . identifying the

raw data from which corrective actions can be developed and implemented.

However, recent issues are evidence that actions in response to self-

assessments have not resulted in substantive improvements.

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Self assessments by maintenance, in conjunction with other site

information, have provided an accurate picture of the performance of the

maintenance department. A declining trend in the maintenance area was

identified following a more thorough and critical review of self-

assessment and other site information. Corrective actions to address

the identified weaknesses have been developed, most notably in the area

of personnel accountability, human performance, and supervisory

oversight.

However, recent issues are evidence that actions in response

to self assessments have not been fully effective.

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08

Miscellaneous Operations Issues (92901)

08.1 (Closed) Licensee Event Report (LER) 50 328/96-007:

Enaineered Safety

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Feature (ESF) Actuation. Start of the Auxiliary Feedwater System. As a

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Result of Inadeauate Return of Eauipment to Service. This event was

discussed in IR ~50 327, 3 N /96 14.

No new issues were revealed by the

LER.

08.2 (Closed) LER 50 327/96 006: A Failed Couoled Capacitor Potential Device

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Caused Actuation of the Generator Backue/ Transformer Feeder Relav

Triooina the Turbine and the Reactor. This event was discussed in IR

50 327, 328/96 08.

The LER concluded that the most probable cause of

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the coupled capacitor failure was that the lower capacitor module began

to conduct current because of internal degradation. The corrective

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actions described in the LER were reasonable and complete. With the

exception of the arobable cause of the failure, no new issues were

revealed by the LER.

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08.3 (Closed) IFI 50 328/97-01 05:

Review Root Cause Which Led to Notice of

Enforcement Discretion (N0ED) on EDG,

The inspectors monitored the

repair of the 2A A EDG governor actuator as it occurred on February 13-

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15, 1997, and concluded that the failure was not related to any

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maintenance activities performed on the actuator and the licensee could

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not have predicted the failure. Once the failure was identified, the

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licensee worked expeditiously to replace the actuator and subsequently

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used approximately 20 of the 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> which the NRC had approved in the

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extension of the Technical Specification (TS) allowed outage time. The

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actual failure mechanism of the actuator is described in LER 50 327/97-

002.

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(Closed) LER 50 327/97 002: Enforcement Discretion Granted When

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Problems With the 2A A Diesel Generator Actuator Was Identified. The

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request and approval for enforcement discretion was discussed in IR 50-

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327, 328/97 01. As stattd in the IR, the inswctors verified the

licensee's compensatory actions which were tacen during the additional

allowed outage time of the 2A A EDG. The inspectors reviewed the root

causes and the corrective actions related to the governor actuator

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failure, as described in the LER, and determined that they were

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reasonable and complete.

No similar problems were identified.

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II. Maintenance

M1

Conduct of Maintenance (61700, 61726, 62703, 62707, 64704)

M1.1 General Comments

a.

Inspection Scope

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The inspectors observed and/or reviewed all or portions of the following

work activities and/or surveillances:

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2 SI ICC 003 039.3

Channel Calibration of Steam Generator 1

Level Channel III Rack 11 Loop L 3-39

(L518)

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WO 97 008251 000

Replace Eagle Input /0utput Card

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0 SI 0PS 082 007.M

Diesel Generator Surveillance Frequency

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2-SI 0PS 082 007.B

Electrical Power System Diesel Generator

2B B

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0 SI SXV-003 243.0

Full Stroke Testing of Check Valves 0 3-

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894 and 0 3 895

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1 SI-SXP 003-201.B

Motor Driven Auxiliary Feed Water Pump

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1B B Performance Test

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1-SI-0PS 082-007.B

Electrical Power System Diesel Generator

1B B

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SI-102 M/M

Diesel Generator Monthly Mechanical

Inspections

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0 PI-SXP 018 007.4

Diesel Generator 18 B Fuel Oil transfer

Pump Performance Test

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0-SI CPS 067-682.H

ERCW Flow Balance Valve Position

Verification

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0 SI-SXV 067 245.3

Full Stroking of the 1B B DG ERCW Check

Valves

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1-S0 2/3 1

Condensate and Feedwater System

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1 SI-SXV 000 004.0

Remote Valve Position Indication

Verification

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0 SI SXV-001 266.0

ASME Section XI Testing (TDAFW Trip and

Throttle Valve)

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1 SI 0PS 082 007.A

Electrical Power System Diesel Generator

1A A

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0 SI-SXV 062 266.0

ASME Section XI Testing (Letdown Isolation

Valve)

b.

Observations and Findinos

The inspectors noted that the work activities and the 3erformance of

surveillance activities were adequately performed, wit 1 the exception of

the TDAFW surveillances documented in Section E2.2.

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M1.2 Failure of EDG 2A A

a.

Inspection Scope

The inspector reviewed the engineering, maintenance and testing

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activities associated with the repair of the 2A A EDG following a

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generator fault during the monthly surveillance test.

b.

Observations and Findinas

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During the monthly surveillance test of the 2A A EDG, the 2A A EDG

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tripped and the instantaneous overcurrent and differential current

arotective relays picked up.

Observers in the diesel generator room

1eard a " boom," felt the air compression, and noted a puff of smoke from

the diesel generator.

,

Subsequently, the licensee developed an extensive troubleshooting plan

to identify the generator fault.

Initial meggaring and testing failed

to identify any problem, so the generator housing was disassembled for

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visual inspections. The fault was eventually identified as a phase to

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phase short as a result of previous maintenance activities.

It was

swculated that during cable replacement activities in February 1997,

tlat the stator insulation was cracked leading to the fault.

In

addition, the fault occurred at a point where a tie wrap was used to tie

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off the replacement cables to the stator and the use of the tie wrap was

being questioned.

The inspector observed the licensee's troubleshooting activities and the

planning for those activities. The inspector noted that the maintenance

manager, with assistance from engineering, developed an extensive

troubleshooting plan: and following identification of the fault,

developed an extensive retesting program for ensuring EDG operability.

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The inspector noted that the failure on July 2,1997, was the second

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failure in the last twenty starts and would result in weekly testing of

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the 2A A EDG.

In addition, the July 2, failure was the sixth failure in

the last 100 start attempts and required a 30 day report be' available

for audit (due August 1). A subsequent ammendment to the Technical

Specifications issued July 14, 1997, eliminated the requirements for

increased testing and the 30 day report. An IFI is being identified to

review the licensee's reliability improvement and failure analysis. (IFI

50 327, 328/97-06 03),

c.

Conclusions

An IFI was identified to review the licensee's reliability and failure

analysis.

A positive observation was noted with the extensive troubleshooting plan

and post maintenance testing plan developed by the maintenance manager

with the support of engineering.

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M1.3 Reclacement of Unit 2 Looo 2 Steam Generator Level Controller

a.

Insoection Scope

The inspector observed the replacement of the Unit 2 Loop 2 steam

generator level controller on June 12, 1997.

b.

Observations and Findinos

The inspector attended the pre job briefing and observed portions of the

actual replacement of the Unit 2 Loop 2 steam generator level

controller. The controller had a recent history of periodically

drifting which would result in steam generator level increases as large

as 7%. These level deviations were documented in IR 50 327, 328/97 04.

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The controller replacement was performed under Work Order (WO) 97-

006224. The pre job briefing was thorough and the replacement of the

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controller by instrument maintenance personnel was carefully performed.

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Operators involved in the evolution had received special training on the

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Sequoyah simulator prior to the controller replacement. The entire

evolution was well planned and executed.

No further problems were noted

during the inspection period.

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M1.4 Review of Fire Barrier Visual Insoections

a.

InsDection Scooe

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The inspector reviewed work request (WR) C386982, WO-97007232, and 0 SI-

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FPU 302-001.R. Fire Barrier Visual Inspection Auxiliary Building

Elevation 690 and Below, Revision 0, and 0 SI-FPU 302 002.R. Fire

Barrier Visual Inspection Auxiliary Building Elevation 706 and Above,

Revision 0, regarding the licensee's visual inspections of fire barriers

and penetrations of fire barriers in the auxiliary building.

b.

Observations and Findinas

On April 8,1997, the licensee initiated WR C386982 to inspect the fire

sealant material in nine penetrations located in the auxiliary building.

The licensee's inspection of these nine penetrations was part of a

larger scope inspection of numerous penetrations. The purpose of the

inspection was to ensure that the penetrations met the design drawing

descriptions. Each penetration inspected had a unique penetration

number for each end of the penetration. WR C386982 listed both

identification numbers for each of the nine penetrations to be

ins >ected. The WR stated that the penetrations were to be inspected on

)

bot 1 sides of the penetration for an evaluation of penetration seal type

and integrity.

Enough insulation on both sides of the penetrations was

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to be removed such that the depth and condition of the fire sealant

material in the penetration could be inspected.

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On May 3, 1997, the licensee initiated WO 97007232 to inspect and rework

the nine mechanical / electrical penetration seals identified in WR

C386982. However, the WO only listed the identification number for one

side of each of the nine penetrations and did not specify that both

sides of the each penetration were to be inspected. The W0 directed

that the pre and aost maintenance testing should be performed using

0-SI FPU 302-001.1 and 0 SI FPU 302 002.R.

Both of the sis, in Step

6.2, directed that the fire barriers were to be inspected on both sides

of walls, floors, hatch covers and ceiling as listed in Appendix A of

the SI.

On May 13, 1997, a maintenance technician visually inspected each of the

nine penetrations.

However, the technician only inspected the one side

listed in the W0. On the SI data sheet associated with each

penetration, the technician wrote "na" (not-applicable) for the

penetration side which was not inspected. The technician apparently

followed the specific instructions in the W0, which only listed one side

of each penetration, and in doing so, failed to comaly with the

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requirements of the SI to inspect both sides of eac1 penetration.

On June 14, 1997, WO 97007232 was signed off as being completed.

However, on June 20, 1997, one of the foreman assigned to the fire

penetrations inspection, while reviewing his notes, discovered that-one

of the penetrations needed additional inspection / work. He then took

steps to retrieve the closed W0 and to reinspect the penetration in

question (penetration number A06690W0034).

On June 25, 1997, the inspector accompanied the licensee to inspect

penetration number A06690W0034 and verified that the penetration

contained ',ess than the required 12 inches of insulation.

PER No.

SQ971629PER was written to document that the fire barrier contained less

than the minimum required insulation. Although the licensee determined

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that the penetration still met the requirement for a 1 / hour fire

barrier,additionalsealantwasaddedtomeetthe12incilesrequirement.

The licensee also questioned whether other penetrations had been

inadequately inspected and, as a corrective action, reinspected 100% of

the previously inspected penetrations (138 penetrations).

c.

Conclusions

The inspector determined that the licensee failed to inspect both sides

of nine fire barrier penetration seals as required by procedures 0 SI-

FPU 302 001.R and 0 SI FPU-302 002.R and failed to identify that one of

the nine penetrations contained less than the recuired amount of sealant

material. This licensee identified and correctec violation is being

treated as an NCV, consistent with Section VII.B.1 of the NRC

Enforcement Policy (NCV 50 328/97 06 04). A contributing factor to this

NCV was WO 97007232 did not specify that both sides of fire barrier

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penetrations be inspected.

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M2

Maintenance and Material Condition of Facilities and Equipment (62707)

M2.1 Plant Housekeepina Condition Imorovements

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a.

Insoection Scope

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The inspectors observed the housekeeping of the facilities during

routine plant observations,

b.

Observations and Findinas

)

During routine plant walkdowns the inspectors observed the housekeeping

condition of the units. Specifically, significant im)rovements in

housekeeping over the last six months were noted in t1e turbine building

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for both units. This included painting, cleaning and removal of

equipment and debris.

In addition, the improvements were made following

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significant work in the turbine building for condenser tube replacements

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during the recent Unit 1 outage. The licensee's efforts were continuing

and were addressing other areas of the plant.

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Conclusions

A positive observation was noted with housekeeping improvement noted in

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the turbine building.

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M4

Maintenance Staff Knowledge and Performance (61700, 62707)

M4.1 Imoroner Work Activities On the Unit 2 Excess Letdown Isolation Valve

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a.

Insoection Scope

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The inspector reviewed the maintenance and operation activities

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associated with the repair of the Unit 2 letdown isolation valve and the

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improper maintenance activities performed on the Unit 2 excess letdown

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isolation valve.

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b.

Observations and Findinas

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At 1:47 p.m., on June 6,1997, the Unit 2 reactor coolant system letdown

isolation valve failed closed. At 1:59 p.m., excess letdown was placed

in service.

Subsecuently, reactor power was decreased to approximately

30% in order to recuce the area radiation levels so that personnel could

enter the reactor building and inspect the letdown isolation valve.

During the ins >ection, maintenance noted that the ASCO solenoid valve

associated wit 1 the letdown isolation valve had failed.

WRs were initiated to make the appropriate repairs, management oversight

was assigned, and the maintenance workers were taken to Watts Bar Unit 2

to observe the location of the valve in containment.

In addition, prior

to the start of the work activities, detailed pre job briefings were

held with workers and supervisors.

Initial containment entries were

made and the scope of the maintenance activities was determined. Health

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physics personnel accompanied the workers into the radiation areas and

appropriate stay times were provided.

Following the initial entry by maintenance workers with a management

observer, different maintenance workers entered containment to

disassemble the letdown isolation valve (2 FCV 62 69). The management

observer did not go to the work location with the workers during the

initial disassembly. Approximately 10 minutes after the start of the

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work activities, the Unit 2 control room operator noted that the valve

indicator lights for the excess letdown isolation valve (2-FCV 62 54)

had gone out and that the pressurizer level had decreased. The

maintenance job supervisor was called and asked to verify maintenance

activities on the correct valve.

It was determined that the maintenance

workers had started work on the wrong valve. The excess letdown valve

was reassembled and operations reestablished excess letdown flow and

recovered pressurizer level.

The NRC resident inspector was observing control room activities during

this evolution and noted that the control room operators did an

excellent job in identifying the improper work activities. There were

no alarm functions to warn the operators of the loss of excess letdown

and if disassembly of the excess letdown valve actuator / operator had

progressed, a high level pressurizer trip could have occurred.

Following the reassembly of the excess letdown valve, the maintenance

workers were debriefed by plant management.

It was determined that the

pre job briefing had not identified the fact that there were two similar

valves in the work area. The inspector considered the most significant

deficiency was that although extensively trained in "self checking

techniques " the maintenance workers had failed to self check that they

were on the correct valve prior to starting work.

In this event, the licensee considered this work to be a " sensitive"

activity, extensive pre job briefs were conducted, on the job

observation of the work area was conducted at Watts Bar Unit 2,

management oversight was provided, and the valves were clearly tagged;

however, the workers did not verify the valve identification tags prior

to starting work. The failure to work on the correct valve is

considered to be a failure to follow the maintenance W0 and is

considered to be a violation.

The inspector noted that operations did an excellent job in identifying

that work was being performed on the wrong valve and subsequently,

maintenance did a good job in using positive reinforcement in dealing

with this event by having the responsible manager and workers brief the

rest of the maintenance staff and the NRC, on the human performance

errors that led to this event. This licensee-identified and corrected

violation is being treated as an NCV, consistent with Section VII.B.1 of

the NRC Enforcement Policy (NCV 50 328/97 06-05).

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Subsequently, the licensee restarted repair activities for the letdown

isolation valve. The ASCO solenoid was found to be degraded and was

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replaced; the air supply regulator was found maintaining air supply

pressure at the wrong pressure (low) and was readjusted to ap3roximately

60 asig; this resulted in failure of the valve diaphragm whic1 then had

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to >e replaced.

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C.

Conclusions

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One NCV was identified for failure to follow maintenance instructions.

A positive observation was noted for operations timely identification of

improper work activities on the excess letdown valve.

M4.2 Testina of Safety Related Loaic Circuits

a.

Inspection Scope

Generic Letter (GL) 96-01, Testing of Safety Related Logic Circuits, was

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issued by the NRC to address problems in the industry with the testing

of safety related logic circuits required by TSs. GL 96 01 required

licensees to compare schematic drawings and logic diagrams to

surveillance procedures for those systems to ensure that existing

s

testing was adequate to satisfy TS surveillance requirements (SR).

The ins)ector reviewed licensee actions associated with GL 96 01 for

Sequoyal. This review included a review of the licensee's disposition

of various issues identified by the licensee during their review.

Additionally, the inspector selected various SRs and verified that the

licensee's surveillance testing program was adequate and that the

associated SR was satisfied.

b.

Observations and Findinas

The inspector reviewed the Sequoyah GL 96 01 Review Report, which was

issued on May 5, 1997. This report documented the licensee's review

effort in this area along with disposition of the various issues

identified during the review. The inspector determined that three

separate examples of TS SRs which were not satisfied by existing sis had

been identified by the licensee as the result of the GL 96 01 review.

Three PERs were generated to document these TS SR violations which

resulted in issuance of two LERs, 50 327/97 003 and 50 327/97 008. One

other example of an inadequate SI had been identified by the licensee's

T&PS group prior to the GL 96-01 review and was addressed separately in

the licensee's May 5, 1997 GL 96 01 Report. That issue was described

in LER 50 327/97 001. The inspector reviewed these three LERs and

determined that the licensee's corrective actions were adequate. These

LERs are discussed in more detail in Sections M8.5, M8.6, and M8.7 of

this report. The licensee had attributed the failure in each case to

inadequate sis.

For each case the appropriate limiting condition for

operation (LCO) was entered, required testing performed and the

associated SI revised. The licensee failed to perform adequate

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surveillance testing, however this is being treated as an NCV,

consistent with Section VII.B.1 of the NRC Enforcement Policy (NCV 50-

327, 328/97-06 06, Failure to Properly Perform Surveillance Testing).

.

The inspector noted that the licensee had also identified numerous other

.

'

examples of sis which failed to test all attributes of the logic

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circuits.

In all of those examples the licensee had determined that

although the procedures required revision to test all attributes of the -

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logic circuits, existing testing had satisfied the language in TS.

In

each of those cases licensee personnel had documented the specific issue

in the GL 96 01 Review Report. These issues resulted in 11 additional

^

' PERs associated with 37 required SI >rocedure changes, five needed TS

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change requests, and a required UFSAl change. The inspector selected

several of those issues for detailed review to determine the adequacy of

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the licensee's corrective actions. No problems were identified with the

licensee's disposition of those issues. The inspector determined that

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significant corrective actions were taken, or were in the process of

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being completed by the licensee for the deficiencies identified by the

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licensee in the May 5, 1997, GL 96 01 Report.

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c.

Conclusions

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The licensee's GL 96 01 review identified several inadequate sis along

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with needed UFSAR and TS revisions. This included four examples of SRs

no' satisfied and an NCV for failure to perform required TS surveillance

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te ting was issued. Significant corrective actions were taken, or were

in the process of being completed by the licensee for the deficiencies

identified by the licensee in the May 5,1997, GL 96 01 Report.

M4.3 Surveillance Testina

a.

Insoection Scope

The inspector selected several protective instrumentation and engineered

safety features actuation system (ESFAS) SRs for calibration and

functional testing and verified that actual testing performed during the

recently completed refueling outage and two recent forced outages had

satisfied the SRs.

b.

Observations and Findinas

The inspector selected several TS SRs for review of existing licensee SI

procedures to verify that the testing satisfied the SR. Those SRs

selected included various protective instrumentation and ESFAS SRs for

calibration and functional testing from TS Tables 4.3.1 & 4.3.2.

The

inspector reviewed the associated licensee sis and verified that the

instructions satisfied the SRs.

Additionally, the inspector reviewed various SRs from TS Tables 4.3.1

and 4.3.2 and verified that actual testing performed during unit outages

had satisfied the SRs. Specifically, the inspector verified that the 18

month channel calibrations required by SRs 4.3.1.1.1 and 4.3.1.1.2 for

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reactor coolant pump (RCP) undervoltage, RCP underfrequency, and reactor

trip system interlocks and containment ventilation isolation testing

required by SRc 4.3.1.1.1,.4.3.1.1.2, and 4.9.9 were performed as

required during the recent refueling outage in March 1997.

.

Additionally, the inspector verified that the functional testing

requirements of SR 4.3.1.1.2 for the reactor trip system interlocks had

been satisfied prior to reactor startup following that refueling outage

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and from the forced outages in June 1996 and November 1996.

SR

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4.3.1.1.2 required that the logic for interlocks shall be demonstrated

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operable prior to each reactor startup unless wrformed during the

preceding 92 days. The inspector noted that t1e licensee's surveillance

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testing program required the reactor trip system interlocks to be tested

such that each train was functionally tested every 62 days on a

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staggered test basis.

No problems were identified during this review.

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c.

Conclusions

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For each TS SR reviewed by the inspector, the licensee had performed

required surveillance testing during the March 1997 refueling outage,

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and prior to reactor startup following the forced outages in June 1996

and November 1996.

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Miscellaneous Maintenance Issues (92902)

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M8.1 (Closed) VIO 50-327. 328/96 02 05:

Failure to Control Imolementation of

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Plant Modifications as Reauired By SSP 9.3.

As discussed in IR 50 327,

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328/96 08, the inspector had verified the corrective actions and

concurred with the licensee's root cause determination as described in

the licensee's response letter dated May 22, 1996.

However, at the

time of that review, the licensee's corrective actions were not

complete. The licensee had committed in their response letter to

evaluate the effectiveness of the actions in resolving site human

performance issues. That evaluation, Assessment NA SQ 96 26, was

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completed on October 31, 1996, and concluded that while improvement had

been achieved, the corrective actions had not resulted in the desired

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level of human performance. The evaluation recommended, and the

licensee implemented, a consistent site-wide peer evaluation process.

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The inspector determined that the licensee addressed the procedure

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problems associated with controlling plant modifications, and concurred

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with Nuclear Assurance's assessment that the desired level of

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performance has not yet been achieved.

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M8.2 (Closed) VIO 50 327. 328/96 12 01:

Failure to Revise Emeraency

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Operatina Procedures as a Result of Desian Chanaes to Abandon Plant

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Eauioment. The inspector verified the corrective actions described in

the licensee's response letter, dated February 3,1997, to be reasonable

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and complete. No additional problems were identified during the

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inspector's review.

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M8.3 (Closed) LER 50-328/96 003:

Reactor Trio Breakers Were Manually Doened

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With An Automatic Generation of a Feedwater Isolation Sional and a

Manual Reactor Trio.

This event was discussed in IR 50 327, 328/96 05.

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No new issues were revealed by the LER.

.

M8.4 (Closed) LER 50-328/96-006: Automatic Reactor Trio of the loss of Power

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to Start Bus 2A. the Start of Four Emeraency Diesel Generators. and

Loadino of Emeroency Diesel Generator 2B 3.

This event was discussed in

IR 50 327, 328/96 14.

In addition to the LER, the licensee initiated

PER No. SQ963132PER which required a root cause investigation. That

investigation considered several root cause possibilities but was not

able to determine the cause of the breaker opening.

M8.5 (Closed) LER 50-327/97 001:

Failure to ProDerly Perform Surveillance

Testino on the EDG Start Timer Relays that are Contained in the Start

Loaic Circuity.

This deficiency was identified by the licensee's T&PS

group prior to the GL 96 01 integration review phase and was addressed

separately in the May 5, 1997, GL 96 01 Re art. The licensee determined

that only one of the two channels of the EXi start timer relay circuitry

per shutdown board had been tested under the existing SI. The inspector

reviewed PER No. SQ970161PER along with other documentation provided by

the licensee and verified that operations personnel had entered the

-appropriate LC0 for Units 1 and 2 on January 25,-1997, and testing

.

performed to test both channels of the start timer logic prior to

exiting the LCO. The inspector noted that the appropriate SI was

revised and that subsequent testing verified the as-found condition of

each channel to be acceptable.

M8.6 LClosed) LER 50 327/97 003:

Failure to Properly Perform Surveillance

Testina on the Centrifuaal Charaina Pumo Inlet Isolation Valve Loaic.

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This deficiency was identified by the licensee as Issue Number 3 in the

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May 5, 1997. GL 96-01 Report. The licensee determined that surveillance

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testing of the centrifugal charging pump inlet isolation valve interlock

had not been performed as required by TS 3.5.2.a and 3.1.2.2.

Each

volume control tank isolation valve had two parallel electrical

initiation paths and the existing SI had not independently verified both

paths. The inspector reviewed PER No. SQ970442PER along with other

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documentation provided by the licensee and verified that operations

personnel had entered the appropriate LC0 for Units 1 and 2 on March 5,

1997, and special testing performed to test the individual contacts in

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each of the two parallel circuits prior to exiting the LCO. The

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inspector noted that the appropriate SI was revised and that the special

testing verified the +found condition of each channel to be

acceptable.

.

M8.7 (Closed) LER 50 327/97 008:

Failure to Properly Perform Surveillance

~

Testino on the Containment Air Return Fan Start Loaic and on the

Blackout and Auto Seauencino of the Station Fire Pumos. These two

deficiencies were identified by the licensee as Issues Number 13 and 14

in the May 5, 1997, GL 96 01 Report. The licensee determined that

.

surveillance testing of the blackout and auto sequencing timer circuit

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for the station fire pumps and the containment air return fan auto start

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logic had been inadequate to satisfy TS 3.8.1.2 and 3.6.5.6.

Surveillance testing of the station fire pumps used a handswitch and had

not independently verified the blackout auto sequencing circuit which

was parallel to the handswitch.

Surveillance testing of the containment

air return fans had not verified the correct o>eration of the solid

state protection system (SSPS) contacts which 1ad been jum)ered to

simulate the auto start signal. The inspector reviewed PEl No.s

SQ970610PER and SQ970611PER along with other documentation provided by

the licensee and verified that operations aersonnel had entered the

appropriate LCOs for Units 1 and 2 on Marc 1 25, 1997, and special

testing performed to test the blackout auto sequencing circuit and the

SSPS contacts for the containment air return fans prior to exiting the

LCOs. The inspector noted that the appropriate sis were revised and

that the special testing verified the as found condition of each logic

circuit to be acceptable.

M8.8 (Closed) IFI 50 327. 328/94 30 01: Deficiencies in Check Valve Proaram

Imolementation. This item identified weaknesses in the licensee's

implementation of its check valve program. These weaknesses included a

failure to issue quarterly reports specified by the program, failure to

update the check valve database, and incorrect flow disturbance

locations recorded in the check valve database.

In a letter dated

December 13, 1994, the licensee informed the NRC of the causes of the

weaknesses and of actions being taken to address the weaknesses. The

inspectors verified completion of the actions stated in the letter,

including PER No. SQ940772PER, which was initiated to develop corrective

actions and resolve the condition.

M8.9 (Closed) IFI 50-327. 328/94 30-02:

Inadeauate Preventive Maintenance on

Reach Rod Valves. This item identified weaknesses in the preventive

maintenance performed for reach rod valves. As a result of omission of

testing following preventive maintenance, a reach rod valve had remained

open and resulted in the loss of a large volume of water.

Position

indication on such valves was inaccurate, making it difficult to

determine when a valve was closed.

In a letter dated December 13, 1994,

the licensee informed the NRC of the causes and the actions being taken

to address the weaknesses.

The inspectors verified completion of the

actions stated in the letter, which included revisions to preventive

maintenance instructions to require post maintenance stroking,

development of corrective actions through PER No. SQ940106PER, and

issuance of an order instructing operations personnel not to rely on the

position indicators of reach rods.

M8.10 (Closed) IFI 50 327. 328/94 22 02:

Snubber Desian and Maintenance

Items.

This item identified aerceived snubber design setting and

maintenance problems for furtier review. The inspectors found that the

licensee had prepared a paper regarding snubber inspections that

res>onded to these perceived problems. This paper was entitled.

Tec1nical Specification and ASME Section XI Inspection for Sequoyah

Snubbers, and was dated October 1994.

Explanations provided in this

document were reviewed by the inspectors and considered adequate to

allay the original concerns.

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III. Enaineerina

El

Conduct of Engineering (37550, 37551)

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El.1 GL 89 10 Proaram Implementation

a.

Insoection Scope (Temocrary Instruction 2515/109)

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This inspection provided an assessment of the licensee's implementation

of GL 8910, Safety Related Motor-0perated Valve Testing and

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Surveillance. The licensee notified the NRC that they had completed

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implementation of GL 8910 in letters dated December 11, 1995 (Unit 1)

and July 1,1996 (Unit 2).

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The assessment included the scope of motor-operated valves (MOV) in the

licensee's program, determinations of M0V settings and verifications of

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MOV capabilities, periodic verification of M0V capabilities, M0V

corrective actions and trending, M0V post maintenance and post

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modification testing, and actions to address pressure locking and

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thermal binding. The NRC inspectors conducted the assessment through a

review of the licensee's GL 8910 implementing documentation and through

interviews with licensee oersonnel. The documents reviewed included:

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Site Standard Practice SS)-6.61, Motor Operated Valve Program / Generic-

Letter 89 10, Revision 1: Standard Engineering Procedure DS M18.2.21,

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Motor Operated Valve Thrust and Torque Calculation, Revision 8; and the

calculations, test records, etc., referred to in the following

3aragraphs.

In addition, the inspectors reviewed summary tabulations of

40V information and calculation results prepared by the licensee.

Prominent among the tabulations was a list of "available valve factors"

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(AVFs) for the licensee's GL 8910 gate valves. The licensee prepared

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this list at the inspectors * request to aid them in assessing the

capabilities of the licensee's MOVs. The AVFs were calculated using

formulas described in previous NRC irs (e. g., IR 50 338, 339/97-01,

dated March 21, 1997). The inspectors compared the AVFs for the

licensee's valves to valve factor requirements established in industry

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testing which the NRC had previously reviewed. These comparisons were

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performed to determine if the AVFs were conservatively higher.

.

As part of the inspection, the inspectors performed detailed reviews of

special test packages and engineering evaluations which the licensee had

developed for the following sample of M0Vs:

1-FCV 001 018

Turbine Driven Auxiliary Feedwater Pump Steam

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Isolation

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1-FCV-003 136A

Essential Raw Cooling Water (ERCW) Isolation

1 FCV 003 136B

ERCW Isolation

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1-FCV 026 243

Reactor Coolant Pump (RCP) Spray Isolation

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1 FCV 70 090

RCP Thermal Barrier Return Containment Isolation

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2 FCV 003 047

Steam Generator No. 2 Feedwater Isolation

2 FCV 068 332

Reactor Coolant System Pressurizer Block

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b.

Observations and Findinas

1.

Scooe of MOVs Included in the Procram

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The scope of valves included in the licensee's GL 8910 program was

originally reviewd and determined acceptable by the NRC during

Inspection 50-327, 328/91 18. At that time, the scope consisted of 278

4

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MOVs.

In the current inspection the inspectors found that the licensee

'

had subsequently reduced the scope by 53 MOVs. The current program

scope included 138 gate valves,16 globe valves, and 71 butterfly valves

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for a total of 225 valves.

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The bases for the removal of the 53 valves referred to above, were

documented in Calculation EPM RJP 061091, Revision 6.

The inspectors

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found that the bases given were satisfactory, except in the case of 24

plug valves. These plug valves performed supply and discharge isolation

functions in emergency raw cooling water lines for the upper containment

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vent coolers. Their removal from the licensee's GL 89 10 program was

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based largely on a GL 8910, Supplement -1, statement that the types of

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MOVs covered by GL 8910 included gate, globe, and butterfly valves.

The inspectors noted that, while GL 89 10 focused on gate, globe, and

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butterfly valves; it did not exclude plug valves.

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As noted above, the ins wetors did not agree with the bases given by the

licensee for removing t1e plug valves from the GL 8910 program.

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However, based on the design of these valves and on the operation,

testing, and preventive maintenance that the licensee provided: the

inspectors considered the capabilities of these valve adequately

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verified to meet the intent of GL 8910. The plug valves were small

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two inch quarter turn valves, their design resulted in minimal operating

torque requirements under flow conditions, and they were limit

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controlled to obtain full motor capability during' operation. They were

operated under flow conditions on occasion and were stroke timed

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quarterly.

Preventive maintenance was specified every three refueling

cycles and consisted of monitoring motor current, inspecting torque and

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limit switches, monitoring switch actuation, cycling the valve, cleaning

.

electrical contacts, and inspecting actuator lubricant.

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2.

Determinations of Settinas and Verifications of Capabilities for

Gate. Globe. and Butterfly Valves

I

Switch Settinas

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The licensee controlled the operation of gate and globe valves through a

combination of torque and limit switches. The torque switch was

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bypassed in the closing direction for 95 to 98% of stroke length, based

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on handwheel turns. .For opening, the torque switch was bypassed for the

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entire stroke. Butterfly valves were limit switch controlled in both

directions.

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The licensee calculated the predicted thrust and torque to operate gate

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and globe valves using standard industry equations. The predicted

thrust requirements for gate valves were calculated assuming a 0.4 valve

factor with a 20% safety _ factor.

For globe valves, the licensee assumed

a valve factor of 1.0 for closing and 1.2 for opening. Diagnostic error

and torque' switch repeatability were accounted for in the switch setting

calculations. The licensee obtained the predicted torque required to

operate butterfly valves from the valve manufacturers.

The licensee _ established settings for gate and globe valves through a

process that reconciled the predicted operating requirements calculated

for the valves with results obtained from testing valves at Sequoyah or

Watts Bar, or results from the M0V

3rogram conducted by the Electric

Power Research Institute (EPRI). T1e licensee did not use information

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from other utilities in this process because of concern regarding the

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reliability of that information.

The thrust settings for Sequoyah's gate and globe valves were specified

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on setting drawings. The licensee informed the inspectors that these

drawings and the related design calculation packages had not been-

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revised to incorporate all of the most recent setting limits established

in the reconciliation process. Although the valves were currently set

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to values determined acceptable through the reconciliation process, the

setting drawings and calculations permitted lower setting limits _ that

might not'be acceptable in some cases.

Licensee personnel stated that

maintenance personnel knew not to lower settings without first checking

with engineering.

However, as the licensee had previously informed the

NRC that implementation of GL 8910 was complete, the inspectors

expressed concern that the settings and calculations had not been

updated and that more definitive controls were not in place.

In

response, the licensee issued change 97 0525 (dated June 12, 1997) to

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Procedure 0 MI-EMV 317-144.0, Procedure for Testing Motor Operated-

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Valves Using M0 VATS Signature Analysis System, requiring licensee

personnel to contact Site Engineering to determine appropriate switch

settings rather than applying information from the setting drawings.

Further, in a letter dated July 8,1997, the licensee committed to issue

a design change notice (DCN) to update the switch setting sheets after

calculations are completed. The letter stated that this DCN would be

completed for both units by December 1,1997.

The licensee assumed run efficiency in the closing direction when

predicting the torque output capability of its actuators. The

inspectors noted that the actuator manufacturer is

3reparing new

guidelines that might affect the acceptability of t1e licensee's use of

run efficiency.

Licensee personnel stated they were aware of this

situation and had been in contact with the manufacturer. The

manufacturer had provided no guidance but indicated it would be

forthcoming shortly.

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Desian Basis Caoability

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Gate Valves -

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-The design basis capability of Sequoyah's gate valves was established on

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a group by group basis, after dividing the 138 gate valves into 23

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separate groups. The licensee had dynamically. tested 39 of these valves

and the dynamic thrust data was evaluated and extrapolated to design-

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basis conditions for reconciliation with predicted values. Many of the .

23 groups did not include any valves that had been dynamically tested.

F

For these groups, the licensee relied on test data from Watts Bar or the

EPRI program where possible, but in some cases' had obtained no test

data.' The inspectors identified the following issues for resolution:

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The thrust requirements (or valve factors) for gate valve groups 1-8,

10, 14, 18 21, and 23 were not reliable, as they were based on

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insufficient test data. Generally, the requirements for these groups

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were either not supported by any applicable test data or were based on

data from testing a single valve. Also, in the case of group 4, it was

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-not clear whether criteria recommended by-EPRI had been considered in

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extrapolating the opening test data. The licensee demonstrated the

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design basis capability of these gate valves by showing that their-

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available valve factors were reasonably bounding of general industry

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results. The licensee was able to rely on full motor capability in

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determining the available valve factors, since the torque switch was

bypassed for most of the closing stroke. The licensee set-the bypass

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based on handwheel turns and the inspectors questioned the reliability

of this method. The-licensee agreed with this concern and demonstrated

the extent of torque switch bypass for several marginal valves using

diagnostic traces. The licensee used additional justification for M0V

capability where the torque switch was found not to be bypassed into the

valve seating region.

In its letter dated July 8,1997, the licensee-

stated that it would strengthen the group valve factors for its gate

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valves. The letter further stated that industry differential pressure

. test data will be evaluated to justify existing valve factors and that a

group valve factor of 0.6 will be used unless test data supports a

,

different value.

The licensee was relying on information from pump flow testing at

Sequoyah to justify its predictions of thrust requirements for power

operated relief valve block valves 1/2-FCV 68 332/333 (group 7) and had

not addressed the potential effects of blowdown operation.

In its

letter dated July 8,1997, the licensee indicated that further actions

would be taken to justify the capabilities of these valves under

blowdown conditions. These actions included maintenance improvements

(e. g., radiusing internal' valve edges, checking internal clearances,

,

etc.) and a> plying the EPRI PPM (Performance Frediction Model) to

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establish t1e thrust requirements for these block valves. The actions

are to be completed for each unit by the end of their next refueling

outages.

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Containment saray valves 1/2 FCV 72 002 and 039 (group 18) were marginal

in their capaaility, based on available information,

In its letter

dated July 8,1997, the licensee stated that it would verify the flow

orientation of these Aloyco 12-inch split wedge valves and that the

thrust requirements would be predicted using the EPRI PPM or other test

data.

Globe Valves -

The licensee had tested most of its globe valves under dynamic

conditions. This testing demonstrated that all of the licensee's globe

valves were capable of performing their design basis functions.

However, the licensee had not evaluated the adequacy of the closing

valve factor assumption of 1.0 which was used to predict thrust

requirements for its Velan globe valves.

In its letter dated July 8,

1997, the licensee committed to reconcile its closing valve factor

assumption for the Velan globe valves with its test data by

September 30, 1997.

Butterfly Valves -

Sequoyah's butterfly valves were manufactured by Posi-Seal and Pratt.

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The licensee did not calculate predicted torque requirements for

operation of these valves at design basis conditions but obtained the

operating torque requirements from the manufacturers. The butterfly

valves were all limit controlled and the licensee determined that the

capabilities of the valves were well above the specified requirements

(greater than 30%).

The licensee did not consider it practicable to test Sequoyah's

butterfly valves with diagnostics to demonstrate that the operating

torque requirements specified by the manufacturers were satisfactory.

Instead, the licensee used test results from other plants.

The licensee demonstrated the edequacy of the torque requirements

specified for its Posi-Seal valves through tests performed at its Watts

Bar plant. The Sequoyah Posi Seal valves were similar in size to those

tested at Watts Bar and the inspectors found that the Watts Bar data

supported the adequacy of torque requirements specified by the

manufacturer.

The licensee supported the adequacy of the torque requirements specified

for its Pratt butterfly valves based on results from EPRI's testing of a

single 6 inch valve and information obtained from Virginia Power

regarding the results of testing that other licensees had performed on

24 and 36 inch Pratt butterfly valves. Sequoyah had forty two 6 inch

and three 24 inch Pratt butterfly valves but also had 12 ,18 , and 20-

inch sizes. The inspectors did not consider the licensee's information

sufficient to demonstrate the adecuacy of the manufacturer's torque

requirements.

In its letter datec July 8,1997, the licensee stated

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that it would work with Duke Power Company or obtain appropriate test

data from other sources to validate the Pratt requirements.

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. - . - . . -

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Stem Friction Coefficient

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The licensee assumed a stem friction coefficient of 0.15 in its H0V

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calculations. Where subsequent testing of a particular gate or globe

valve indicated a higher value, the licensee assumed the test value in

'

its evaluation of that H0V. The inspectors questioned the reliability

of.the 0.15 stem friction coefficient for the H0Vs that were not

.

i

dynamically tested, as the licensee had not developed a formal

)

evaluation to support the assumption. The_ inspectors evaluated the

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licensee's dynamic test results and found that they supported the

!

assumed 0.15 stem friction coefficient together with a 10% thrust

!

reduction which the licensee assumed to account for rate of loading.

,

!

In reviewing test data for stem friction coefficient and rate of loading

'

effects, the licensee found that the licensee's Velan 1500 lb rated gate

i

i

valves exhibited more severe effects than other gate valves. The-

,

i

licensee evaluated the capability of the valves, using worst case thrust

'

and torque test data from the tested valves for evaluating the valves

'

that were not dynamically tested. This evaluation demonstrated adequate

.

i

capability for the Velan 1500 lb valves.

However, the licensee's

J

calculations indicated that valves 2-FCV 68 332 and 333 (pressurizer.

4

power uperated relief valve block valves) had marginal capability with

F

-

- respect to the torque structural limit.

In its letter to the NRC letter

,

i

dated July 8,1997, the licensee indicated that it would demonstrate

i

[

that these valves greater structural capcbility in revisions to the

related valve calculations.

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Rate of Loadina

The licensee assumed a reduction of 10% in thrust delivered at torque

!

switch trip under dynamic conditions from thrust settings at static

conditions for rate of loading.

In response to inspector questions, the

i

licensee provided test' data to demonstrate that the 10% reduction in

thrust output was reasonable. However, the inspectors found that the

{

licensee had not addressed the ~ potential for reduction in thrust output

i

of the actuator under dynamic conditions when the torque switch was

3

bypassed and operation was controlled by limit switch.

The licensee

i

agreed that it had not addressed this issue and demonstrated that its

!

MOVs operated by the limit switch had sufficient capability with an

L

assumed 10% reduction in thrust output.

In its letter dated July 8,

1997, the licensee committed to provide a 10% rate of loading thrust

F

margin for limit switch control until further evaluation showed a

p

different value was appropriate.

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M0V Dearadation

i

i

The inspectors found that the licensee had not made any provision for

I

degradation of MOVs and brought this to the licensee's attention.

In

J

its letter to the NRC letter dated July 8,1997, the licensee stated it

i

would add a 5% margin as a minimum requirement for MOV degradation.

!

This licensee indicated that this requirement would be incorporated into

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the valve calculations by November 7,1997.

3

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3.

Periodic Verification

,l

The licensee's requirements for periodically' testing GL 89-10 MOVs were

I

' described in Site. Standard Practice SSP 6.61 Revision 1.

SSP 6.61

prescribed testing each M0V statically, as a minimum.

It also indicated

that a sample of GL 89-10 gate valves would be tested under differential

,

pressure conditions until there was technical justification to eliminate

?-

these tests. The inspectors reviewed 3rintouts for 'a sample of M0Vs in

!

the licensee's database and verified t1at the periodic static diagnostic

r

testing of GL 8910 valves had been performed during the last outages

for Unit 1 and 2.

The licensee's periodic verification actions were

i

found to be adequate for closure of GL 8910. The NRC may re assess the

i

licensee's long term periodic verification program as part of its review

'

for GL 96 05, Periodic Verification of Design Basis Capability of

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Safety Related Motor 0perated Valves,

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4.

MOV Trendino

i

The licensee's trending of MOV failures and degradation was previously

reviewed during Inspection 50 327, 328/95 01. That inspection

determined that data was being appropriately collected for trending but

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that there were' no administrative controls specified.

During the

7--

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current inspection, the inspectors found that-the licensee had

i

subsecuently implemented the necessary administrative controls through

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Periocic Instruction 0 PI EMV 317-001.0, Revision 0 (with procedure

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changes 97 507 and 0081). This instruction designated the data to be

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gathered, the required reporting period, responsibilities.for data

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gathering and evaluation, and responsibility for report issuance. The

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licensee's M0V trending was satisfactorily implemented.

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5.

Documentation. Analysis. and Corrective Actions for MOV

l

Dearadation and Failures

I

This area was previously reviewed during Inspection 50-327, 328/95 01,

That. inspection determined that the analyses and corrective actions

1

reviewed were satisfactory but that there were weaknesses in the

j.

document; tion. ~For instance, cause information was not given or was

j

unclear in two cases reviewed. The inspectors reviewed PERs documenting

[

additional examples of MOV failures during the current inspection to

further evaluate the licensee's documentation, analysis, and corrective

'

actions for MOV failures. The examples and the inspectors' findings

l

were as follows:

4

PER No. SQ962636PER

This PER described water damage to main feedwater

'

!:

isolation valve 2-FCV-3 100B. The inspectors found that this PER

3

provided adequate documentation, analysis, and corrective actions for

!

the M0V failure. However, the failure had resulted from a long standing

problem that should have teen recognized and corrected earlier by the

i

licensee. The inspectors learned that the licensee's failure to perform

adecuate evaluations earlier and preclude recurrence of the adverse

-

concition had been previously identified by the NRC as a severity level

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III violation. The violation had been transmitted to the licensee in a

letter dated December 24, 1996.

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PER No. SQ950293PER

This PER described the intermittent failure of

residual heat removal heat exchanger by

valves due to motor contactor problems. pass valve 2 FCV 74 33 and other

The inspectors found that this

,

PER provided adequate documentation, analysis, and corrective actions

'

for the MOV failures. The inspectors observed that the licensee had

experienced similar failures for years but had been previously been

unsuccessful in correction.

PER No. SQ961773PER

This PER described the failure of TDAFW tri) and

l

throttle valve 1 FCV 1-51 to meet its stroke time requirement. T1e

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measured opening time was 8.9 seconds versus a maximum allowed by

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3rocedure of 8.4 seconds, (note: the design allowable was estimated to

3e 20 seconds in a later review). The inspectors found the analysis

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recorded in the PER under the heading " recurrence control"

unsatisfactory.

It first stated that troubleshooting was initiated

without identifying any problems. Then, on a separate continuation

,

,

!

sheet, it went on to indicate that the valve had failed to open the

third time it was cycled for troubleshooting.

The PER postulated that

,

this failure was due to the operator not holding the switch in the open

aosition for a sufficient period of time for the open signal to seal in.

)

iowever, there was no entry of the operator's response to this

conjecture and no supporting evidence of the recorded view.

Licensee

inservice testing personal informed the inspectors that the operator had

been questioned and indicated that he had held the switch in position

until he became concerned that the motor would fail. The operator was

.

reportedly no longer employed at Sequoyah and could not be questioned by

the inspectors. The ins)ectors noted that the troubleshooting following

i

the initial failure of tie valve had apparently been limited to cycling

the valve and checking motor amps. There was no ir.dication that the

licensee either reviewed the available historical test data for this

valve or that diagnostic equipment was considered for troubleshooting

the condition identified. A review of the test data from the last

'

replacement of this actuator would have shown that the stroke time

i

normally measured for this valve during surveillance tests was too short

(less than 6 seconds versus an actual stroke of about 11 seconds).

PER No. SQ970392PER - This PER described another stroke time failure of

valve 1-FCV-1 51 like that referred to in the previous paragraph. The

measured value was 9.5 seconds versus the maximum allowed by procedure

of 8.4 seconds and a normal measurement of 5 to 6 seconds. This

occurred just over 6 months after the previous failure. The licensee's

corrective action for this more recent failure included more precise

testing with diagnostic equi) ment and refurbishment of the valve (note:

only current and time could 3e measured on this valve with the

licensee's diagnostic equipment). The inspectors found that this PER

generally provided adequate documentation, analysis, and corrective

actions for the failure, though some uncertainty remained because the

failure cause was not established. The inspectors noted one entry in

4

the PER which they considered unsatisfactory, involving the adequacy of

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stroke time measurements. The licensee's investigation found that only

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about half the actual stroke time was being measured during surveillance

)

testing due to improperly set indication. The PER indicated that this

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was acceptable as the maximum value specified for the surveillance test

i

was based on deviation from a reference stroke time value and exceeded

no design limit. The entry failed to recognize that the test was

,

(

intended to measure changes over the entire stroke, whereas the licensee

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was only timing about half the stroke.

!

6.

Pressure Lockino and Thermal Bindina

The inspectors reviewed the licensee's GL 95 07 submittals dated

i

February 13, March 15 and August 6, 1966. During the inspection, the

licensee stated that a supplemental response to GL 95 07 would be

submitted to provide pressure locking and actuator capability

calculations for Units 1 and 2 valves FCV 116, FCV-62138, FCV 631,

FCV 63 6, FCV 63 7, FCV-63 25, FCV 63 26, FCV 63 156, FCV 63 157, FCV-

i

68 132, FCV 68 332, FCV 72 2, FCV 72 39, FCV-72 40 and FCV-72 41. The

i

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sup)lemental response would also address the basis for any bonnet

'

leacage assumptions that were used in pressure locking calculations.

The adequacy of the licensee's actions to address pressure locking and

thermal binding remain under NRC evaluation but will be reviewed

.

separately from GL 89-10.

In the future, the NRC staff will address the

adequacy of the licensee's actions in a safety evaluation of the

i

licensee's responses to GL 95 07.

7.

Strenaths

The inspectors observed the following strengths in the licensee's

implementation of GL 8910:

Accurate diagnostic measurements.

'

Personnel who were knowledgeable of the MOV industry issues.

.

c.

Conclusions

Implementation of GL 89-10 at Sequoyah was not sufficiently complete to

permit the NRC to close its review. The licensee had demonstrated that

the current settings and capabilities of the Sequoyah GL 89 10 MOVs were

adequate. However, it had not adequately determined and specified

limitations on the requirements for many of these MOVs to ensure long-

term operability.

In a letter to the NRC dated July 8,1997, the

licensee committed to nine actions to improve its implementation of

GL 89 10. The inspectors considered that these actions, when

sufficiently completed, would resolve the remaining issues regarding the

long term capabilities of Sequoyah MOVs and 3ermit closure of the NRC

review of GL 89-10 implementation at Sequoyal. NRC verification of

!

completion of the actions stated in the licensee's letter of July 8,

1997, was identified as IFI 50 327, 328/97 06 07, Actions to Resolve

Remaining GL 89 10 Issues.

In accordance with its commitment letter,

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the licensee is to notify the NRC of the status of the commitment

actions by the end of 1997.

Weakr. esses were identified in the analyses of stroke time faihres of

i

TDAFW trip and throttle valve 1-FCV 151 documented in two PERL

The inspectors noted two licensee strengths, which are described in

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Section E1.1.b.7.

E2

Engineering Support of Facilities and Equipment (37551)

E2.1 Imorocer Settina of the Safety In.iection System Relief Valves

a.

Inspection Scope

The inspectors reviewed the activities associated with an over pressure

condition of the safety injection system.

In addition, the inspectors

reviewed the American National Standards Institute (ANSI) code

requirements associated with the safety injection system relief valves,

b.

Observations and Findinas

IR 50-327, 328/96 14 discussed a deficient condition which occurred on

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.

November 2, 1995. The Unit 2 operators noted that the safety injection

'

system pressure was indicating 1850 psig and the design pressure for the

system was only 1750 psig. Three system relief valves were available in

the safety injection system and should have relieved system pressure

before exceeding 1805 psig.

Immediately following the event, one of the

relief valves was removed and tested and was found to be set at

approximately 1840 psig. The relief valve was reset to 1750 i3% psig;

however, the other two relief valves were not tested and were not reset,

although the licensee had knowledge from the event that the setpoint

exceeded 3% of the nominal.

The licensee stated that the relief valves were not known to be

functioning outside an acceptable range (6%) as documented in their

relief valve program.

In addition, the corporate TVA QA organization

conducted an assessment of the program and found the program to be

acceptable. The inspectors reviewed the ANSI code requirements and had

concerns with the licensee's interpretations.

Several meetings were

held with the licensee's engineering staff to discuss the ANSI code

requirements.

IFI 328/96 14 01 was identified to follow u) the safety

injection relief valve setpoint issue.

In addition, a Tas( Interface

Agreement (TIA 97 01) was initiated by the resident inspectors and

forwarded to NRC headquarters for review and resolution of the issue.

NRR res)onse to TIA 97 01, Relief Valve Lift Settings Required By

Applica)le Codes (TAC No. M97281) was issued May 21, 1997 and is

l

included as an attachment to this report.

It noted that as left

l

tolerance for setting relief valves is allowed to be as high as 13%.

The as found tolerance should be supported by an analysis of the

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limiting operational or transient events for overpressure or other

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35

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safety parameters to verify that the design limits of the piping,

'

vessel, or system are not exceeded. The overpressure event of

November 2, 1996, is considered by the inspectors to have provided the

licensee with an as-found condition outside i3% and the relief valves

!

should have been reset to with 13%, unless a system analysis existed to

,

support the as found condition for the limiting operational or peak

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transient events for overpressure and other safety parameters to verify

that the design limits of the piping and system are not exceeded. The

TIA also noted that the licensee's arocess of " stacking" the as left and

i

as found tolerances to obtain even ligher allowable limits was improper

and therefore did not appear to conform to the ANSI /American Society of

Hechanical Engineers (ASME) OM 1 code requirements.

Following the November 2 event, on December 5, 1996, the licensee

performed a preliminary system analysis to support leaving the valves in

!

the as-found condition. On January 11, 1997, the licensee submitted a

code interpretation to the National Code Committee. A verbal res]onse

from the committee was received on March 11, 1997, and it noted tlat the

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licensee was not in compliance with the code unless a system analysis

had been performed to support the higher system pressure. On April 4,

1997, the licensee revised the safety injection system relief valve

testing procedure 0-SI-SXV 000 264.0. On June 20, 1997, the licensee

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completed a formal approved system calculation for the safety injection

,

system relief valves. The licensee noted that the subject relief valves

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would be tested during the next Unit 2 refueling outage (Fall 1997).

i

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The inspector noted that the licensee failed to reset the safety

injection relief valves lifting setpoints following the November 2,

1996, event and did not have an analysis to support the as left valve

relief setting. Additionally, it is not clear why 3-out of-3 relief

valves failed to operate within 3% of the nominal setpoint.

Further

review noted that the licensee was not initially in compliance with the

l

ANSI OH-1 requirements for resetting the relief valves or reanalyzing

the system. The licensee's failure to implement adequate corrective

actions to correct the deficient safety injection system relief valves

lifting setpoint is considered to be inadequate corrective actions and

l

is identified as VIO 50 328/97 06 08.

c.

Conclusions

i

A violation was identified for the licensee's failure to implement

'

adequate corrective actions to correct the improper setting of the

safety injection system relief valves.

E2.2 Inadecuate Section XI Surveillance Activities

a.

Inspection Scope

The ins)ectors reviewed the activities associated with the failure of

the TDAN trip and throttle valve to properly stroke on the first

attempt during Section XI testing.

In addition, the inspectors reviewed

_

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the two year Section XI remote accuracy surveillance associated with

this valve.

b.

Observations and Findinas

On February 24, 1997, the Unit 1 TDAFW valve (1 FCV-51) failed its

initial stroke test. Subsequent restroking of the valve documented

acceptable stroke times.

Further review noted that this valve had

failed a previous stroke test on June 17, 1996, and that subse

restroking of the valve had provided acceptable stroke times. quentFollowing

the second stroke failure in February 1997, the licensee developed an

extensive troubleshooting plan with potential root causes. During the

l

1997 Unit I refueling outage, the licensee noted problems with the valve

!

internal clearances and subsequently replaced the valve stem, bushings

and valve disc. The valve was successfully tested following the

maintenance activities.

Following the February 24, 1997, stroke failure, the inspectors reviewed

the associated technical operability evaluation. The evaluation noted

that 1 FCV 51 was still operating within the design limits listed in the

UFSAR, but it did not identify the cause for the deviation / failure. The

inspectors also reviewed PER No. SQ961723PER. initiated following the

June 17, 1996, failure to stroke.

Following subsequent local

,

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observations with ric further problems, engineering documented in the PER

that valve 1 FN 51 had failed to stroke as required possibly due to

operator error , but again did not identify the cause for the

deviat ion /f:ilure. The two evaluations were considered to be lacking

be.cause they did not clearly identify and analyze the cause for the

failures.

Following the February 24, 1997, failure, the inspectors performed a

l

walkdown of the Unit 1 and Unit 2 TDAFW pumps and pump rooms. The

~

inspectors noted that the TDAFW trip and throttle valve (1-FCV-51 and 2-

l

FCV 51) position indicators were set differently. The inspectors then

,

reviewed the Section XI test data for both tri) and throttle valves.

l

The data noted that when measured locally, bot 1 valves stroked open in

a) proximately 11 seconds.

It also noted that the Unit 2 trip and

tirottle valve stroked open in approximately 11 seconds when measured

remotely. However, the data documented that the Unit I trip and

,

throttle valve only took 5-6 seconds to open when measured remotely.

'

The licensee was informed of this discrepancy and during the Unit 1,

1997, refueling outage the licensee reset the Unit 1 trip and throttle

valve limit switches.

,

l

Due to the potential misadjustment of the limit switches on 1 FCV 51,

the inspctor reviewed the " Remote Valve Position Indication"

'

surveillance to verify the licensee's program for ensuring the proper

accuracy of valve limit switches. The inspector noted that the

surveillance acceptance criteria only required the remote indication to

>

'

indicate open with the valve fully open and closed with the valve fully

closed.

It did not require the remote indication to accurately indicate

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37

valve position, so in this case, AFW valve 1 FCV 51 remotely indicated

,

100% open with the valve actually at about 50% open.

c.

Conclusion

j

The licensee is reviewing the requirements against their program.

Pending completion this is identified an URI 50 327/97-06 09: Remote

Position Indicator Test.

E2.3 PER No. S0950890PER. MOVs without "T" Drains

j

a.

Insoection Scoce

The inspector reviewed corrective actions developed and implemented for

the above PER in order to verify that condensate drainage into MOV limit

switch compartments (LSC) had been effectively addressed and the

environmental qualification status of the MOVs had been maintained.

b.

Observations and Findinas

TVA established the following design requirement in response to

potential drainage into LSCs through the conduit system because of

condensed steam inside long vertical conduit runs.

Flooding at higher

elevations and containment spray were also considered as sources for

potential drainage.

"T drains must be added to the low point of the limit switch

compartment (LSC) unless it can be determined by field inspection

that one of the following situations exist:

(1) Conduit runs are

installed such that condensation would not drain into the LSC: or

(2) the motor has a T drain located at the low point of the

actuator in such a manner that the motor would also drain the

LSC."

PER No. SQ950890PER was written on July 25, 1995, to document the

identification of 35 MOVs that required field inspections in order to

verify if T drains were required in the LSC. 8ased on the results of

the field inspections it was determined that T drains would be required

'

in the low point of the LSC of the valves.

Installation of the re

T drains were assigned a Master Issues List (MIL) item number MIL # quired

96017

and the PER was closed on February 9,1996 as a required enhancement in

accordance with Appendix G of SSP 3.4, Corrective Action, Revision 14.

On May 8, 1996, TVA management wrote PER No. SQ96961353PER to document

the closure of PER No. SQ950890PER as an enhancement which did not

comply with NRC guidance delineated in GL 9118 for nonconforming

conditions. The licensee determined that because the deficiency

addressed an adverse condition it could not be treated as an enhancement

only. A review of all PERs closed to Appendix G of SSP-3.4 was

performed by TVA management. This review revealed that 27 PERs had been

previously closed with a conflict with the licensing basis still

existing. Twenty six of these PERs represented UFSAR discrepancies.

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TVA's review of the Appendix G documentation also indicated that these

conditions were not considered adverse conditions since there was no

adverse impact on safe plant operation. Additionally, the Appendix G

form did not provide clear guidance concerning what were adverse

conditions.

PER No. SQ961107PER was written to initiate corrective

actions for this licensee finding. Revision of SSP 3.4 to delete the

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use of Appendix G, paragraph f process and clarifying the definition of

!

adverse conditions relative to the guidance of GL 91-18 was completed by

l

the licensee in response to this programmatic deficiency.

,

The inspector reviewed the corrective action that had been

i

completed for the 35 MOVs requiring LSC T drains. The following

'

documents were reviewed during this effort:

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o

Environmental Qualification (EQ) Binder No. SONEQ MOV 003,

Limitorque Actuators Outside Containment with Class RH

Motors, Revision 27.

l

EQ Binder No. SQNEQ H0V 004, Limitorque Actuators Outside

e

Containment with Class B Motors Revision 34.

EQ Binder No. SONEQ MOV 005, Limitorque Actuators Outside

e

Containment with Class B Motors and Brakes, Revision 28.

,

Based on the above review the inspector determined that a Technical

I

Operability Evaluation (T0E), had been wrformed to justify continued

i

operation without the installation of t1e T drains in the LSC until

'

Unit 2 Cycle 8 and Unit 1 Cycle 9 outages. The inspector concluded that

the T0E provided reasonable assurance that the equipment will perform

l

its safety function in its accident environment when called u mn to do

i

so.

Plant modifications DCN No. H 13071A and M 13103A are scleduled to

l

be prepared for installing the T drains in the MOV LSC for Units 2 and 1

I

respectively. The inspector reviewed the scope of both DCNs and

verified that all MOVs listed on Attachment 2 of PER No. SQ950890PER

were included within the scope of the plant modifications.

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c.

Conclusion

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The inspector concluded that the licensee had developed corrective

.

actions for nonconforming MOVs that were consistent with design

!

requirements and NRC's guidance delineated in GL 91 18.

E2.4 Plant Modifications DCN Nos. M8777A and M8780A

a.

Inspection Scope

The inspector reviewed plant modifications DCN No.s M8779A and M8780A in

order to verify that nonconforming conditions involving environmentally

,

qualified equipment were corrected in accordance with the requirements

of the ANSI N45.2.11 1974 design engineering program. The plant

,

modifications were reviewed with special emphasis on (1) the

a

identification of design inputs: (2) the technical adequacy of setpoint

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39

controls and (3) the technical adequacy of safety evaluations performed

in accordance with the requirements of 10 CFR 50.59.

b.

Observations and Findinas

The scope of the above plant modifications consisted of three aarts.

The first part involved addition of temperature detectors in t1e

auxiliary building to detect a high energy line break (HELB). The

second part involved changes to the auxiliary building environment based

on the results of design basis calculation SQN NAL3 007. Interim Normal

Operation Dose for Equipment Qualification Outside the Shield Building:

and the third involved updating the 100 day integrated accident doses

which also included revising the EQ Binders and associated instrument

accuracy calculations for affected areas / components in the auxiliary

building.

The addition of temperature detectors (RTDs) in the residual

heat removal (RHR) Sump rooms (1A A and 1B B), the RHR heat exchanger

room (1A and 1B); t1e chemical and volume control system (CVCS) letdown

heat exchanger room and the boric acid evaporator package rooms (A and

B) were intended to provide the operator with an early detection of a

high temaerature alarm.

Manual isolation of a line break in the RHR

) ump or leat exchanger room or the CVCs heat exchanger room would then

>e initiated by the operator.

If the line break occurred in the CVCS

heat exchanger rooms automatic isolation of the auxiliary steam line

break would occur by closure of valves 0 FCV 12 79 and 82.

Environmental changes in temperature, pressure, humidity, and radiation

in the auxiliary building were addressed by these plant modifications.

Revised category and operating time calculations and instrument loop

accuracy calculations were prepared to demonstrate continued EQ of

various instrument loops. The new instrument loop requirements were

specified in setpoint and scaling documents contained in the DCNs.

Additionally, Environmental Design Criteria SQN DC-V 21.0, was issued

for use and superseded the environmental drawings 47E235 series.

The inspector reviewed the safety assessment / safety evaluation prepared

for the plant modifications in order to verify the technical adequacy

and compliance with the requirements of 10 CFR 50.59. The safety

assessment correctly applied the screening criteria in assessing the

impact of the changes to the plants licensing basis delineated in the

UFSAR and the TSs. Changes to the UFSAR described on the UFSAR Change

Request Form were verified to have been incorporated by amendment 12 to

the UFSAR. The safety evaluation clearly described the changes

implemented within the scope of the plant modifications and concluded

that an unreviewed safety question did not exist because of the design

changes. The inspector concurred with the conclusion documented.

No

deficiencies were identified during this review.

The licensee's approved design engineering program has established

requirements for design inputs to be identified, documented and their

selection reviewed and approved. Changes from specified design inputs

are also required to be identified, approved, documented and controlled.

Design inputs are required to provide detail information which permits

the design activity to be carried out in a correct manner and to provide

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a consistent basis for making design decisions, accom

verification measures, and evaluating design changes.plishing design

Add 1tionally, the

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design process is required to demonstrate an auditable path from

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approved design outputs to the source of the design input. The

inspector chose a random selection of EQ Binders and reviewed selected

environmentally qualified equiment in order to verify that the

environmental parameters for w11ch the equipment was qualified was

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supported by approved design input information. The following design

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basis calculations were reviewed during this effort:

Calculation No. SQNAPS2 119, Auxiliary Building High Energy

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Line Break Mass and Energy Release for Environmental

Analysis Revision 0

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Calculation SQNAPS2121 Environmental Response of Auxiliary

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Building to HELB, Revision 2

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Calculation No. SONNAL3 007, Normal Omration Dose for

Equipment Qualification Outside the S11 eld Building,

Revision 6

Category and Operating Time Calculations

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SQN-0SG7 0027 Residual Heat Removal System (074) 10 CFR 50.49 Category and Operating Time Calculation, Revision 7

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SQN 0SG7 0019, Chemical and Volume Control (062) 10 CFR 50.49 Category and Operating Time Calculation, Revision

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SQN 0SG7 0012. Auxiliary Boiler System (012) 10 CFR 50.49

Category and Operating Time Calculation.-Revision 7

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Based on review of the above calculations the inspector determined that

environmental parameters of temperature, pressure, humidity, and 40 year

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normal radiation doses had been identified for various areas of the

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auxiliary building. The following EQ Binders and the listed equipment

were reviewed to verify that environmental parameters specified in the

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Environmental Design Criteria SON DC V 21.0 for areas in which the

equipment was located were consistent with values delineated in the

above calculations:

.

UNID

E0 binder

0 TS12-91A

SQUEQ ITS 001, R23

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0-TS 12 91B

SQNEQ ITS 001, R23

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2-TS 074 0043

SONEQ ITS 002, R30

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1 TS 074 0044

SQNEQ ITS 002, R30

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1-FCV 62 63

SQNEQ H0V-005, R28

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1 FCV 62-77

SONEQ IZS 001, R35

Based on the above review the inspector concluded that environmental

parameters of temperature, pressure, humidity, and 40 year normal

radiation doses contained in the EQ Binders were consistent with values

specified in the Environmental Design Criteria SQN DC V 21.0. These

values were also supported by the referenced calculations. The Class 1E

equipment listed had also been evaluated to identify its appropriate

category and operating times. A category and operating time was

assigned to each component for each 10 CFR 50.49 event that might create

a harsh environment in the location of that component.

No deficiencies

were identified during the review to establish an auditable trail from

approved design output information for the listed equipment to the

source of the design input.

The licensee performed demonstrated accuracy calculations to determine

the accuracy of instruments located in a harsh environment during loss

of coolant accident /high energy line break (LOCA/HELB) following a

seismic event. The accuracy of the instruments for normal, post seismic

and accident conditions were determined by considering the environmental

parameters tabulated in the design input section of the calculations.

The inspector selected the following demonstrated accuracy calculations

for review in order to evaluate the technical adequacy of set point

controls:

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Demonstrated Accuracy Calculation PS 43 200A, Revision 7

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Demonstrated Accuracy Calculation 1 TS 1 17A, Revision 5

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Demonstrated Accuracy Calculation 0 TS 12 91A, Revision 5

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Demonstrated Accuracy Calculation 1, 2 PDT 65-80, Revision 8

The inspector performed a review of the calculations and verified that

environmental )arameters in the location of the instruments were

consistent wit 1 approved design documents. Additionally, the calculated

accident accuracy values were reviewed to ensure that they had properly

incorporated these parameters in the analysis. The following design

documents were reviewed during this effort:

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SQNP Environmental Design Criteria SON DC V 21.0, Revision 6

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EQ Binder SONEQ ITS 001, Revision 23

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EQ Binder SONEQ XHTR 005, Revision 14

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Based on this review the inspector identified discreaancies in numerical

values of the 100 day integrated accident doses in t1ree calculations.

Discrepancies were identified in calculations 1 TS-1-17A PS-43 200A,

1,2 PDT 65 80 and the values listed in the EQ Binder and/or the

Environmental Design Criteria SQN DC V 21.0. The root cause of this

problem appears to be the incorrect reference to the environmental

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drawings contained in the calculations. These drawings were voided by

SQN DC V-21.0 which now specifies 100 day integrated accident doses

based on 1000 effective full power day average core exposure.

TVA

management was informed of this inspection finding.

PER No. SQ971513PER

dated June 5, 1997 was prepared by TVA to initiate corrective action for

this deficiency.

The inspector verified that the 100 day integrated accident doses in the

EQ Binders were bounded by the test values and that the above equipment

were qualified to the requirements of 10 CFR 50.49.

The inspector

concluded that the demonstrated accuracy calculations were performed

using accepted industry practices and the results were technically

adequate.

c.

Conclusions

The inspector concluded that the 10 CFR 50.59 Safety Evaluations were

technically adequate. Additionally, the design control program was

implemented in accordance with the requirements of ANSI N45.2.111974 in

that there was a clear and auditable path from selected design outputs

back to the source of the design inputs. Set point controls were

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determined to be technically adequate. The overall quality of plant

modifications DCN M8779A and M8780A was determined to be good and

appears to have achieved the design objective of re establishing

configuration control of Sequoyah's EQ program.

E.8

Miscellaneous Engineering Issues (92903)

E8.1 (Closed) VIO 50 327. 328/97-03 02:

Failure to Follow In.structions in a

Work Order Resultina in an ESF Actuation. The inspector verified the

corrective actions described in the licensee's response letter, dated

June 11, 1977, to be reasonable and complete.

No similar problems were

identified.

(Closed) LER 50-327/97 007: Diesel Generator Starts That Resulted From

Cuttina a Cable While Drillina a Panel and Durina Repairs to the Damaaed

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Cable. This LER was closed based on the corrective actions of VIO 50-

327, 328/97 03 02.

No new issues were revealed by the LER.

E8.2 (Closed) LER 50 327/96 004:

Inadvertent Enaineered Safety Feature (ESF)

Actuation. Loss of Power Sianal and Start of Four Diesel Generators.

The inspector reviewed the event which occurred due to a breaker failure

when operators attempted to transfer the 2B start bus from the alternate

to the normal aower su) ply. The inspector concluded that the corrective

actions descriaed in t1e LER were reasonable and complete.

No new

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issues were revealed by the LER.

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E8.3 (Closed) LER 50 327/96-008: A Quarterly Backseat / Closure Test on Five

Check Valves On Each Unit Was Not Performed As Recuired By the American

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Society of Mechanical Enaineers (ASME)Section XI In Service Valve

Testina Proaram Basis Document.

This issue was discussed in IR 50 32'7,

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328/96 08 and resulted in the issuance of NCV 50 327, 328/96 08 03.

No

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new issues were revealed by the LER.

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E8.4 (Closed) LER 50 327/96-009: An Auxiliary Buildina Secondary Containment

Boundary / Fire Barrier Was Not Maintained as Reauired by Desian Resultina

From a Failure to Follow the Desian Control Process. This LER was a

minor issue and was closed.

E8.5 (Closed) IFI 50 327. 328/96 14 02: Review Corrective Actions Related to

Continuina Steam Dumo System Operational Problems.

(Closed) IFI 50 327. 328/96 17 03: Steam Dumo Drain System

Imorovements.

The above two IFIs discussed problems related to the operation of the

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steam dump systems on both units. Proposed corrective actions were

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developed and were documented in IR 50 327, 328/97 17. During the Unit

1 outage, the licensee implemented various modifications to the steam

dump system. The success of the modifications was discussed in IR 50

327, 328/97 04 Section E2.1. Walkdowns of the steam dump system during

startup noted that the modifications had corrected the mild water

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hammering, observed during previous startups and shutdowns.

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E8.6 (Closed) 1.ER 50 328/96 004: After a Reactor Trio Breaker Was Removed.

It Was Found To Have Inocerable Auxiliary Contacts.

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(Closed) LER 50 328/96 004. Revision 01: After a Reactor Trio Breaker

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Was Removed. It Was Found To Have InoDerable Auxiliary Contacts,

The above two LERs discussed the inadequate maintenance activities

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associated with the on line refurbishment of the Unit 2 "B" reactor trip

breaker and the subsequent installation of that breaker into the reactor

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3rotection system.

IR 50 327, 328/96 13 identified apparent violations

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EEI 96 13-07. EEI 96-13 08, and EEI 96 13 09, which were subsequently

documented as escalated enforcement action EA 96 414. The corrective

actions associated with these LERs will be reviewed and documented

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during the followup of EA 96 414.

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E8.7 (Closed) IFI 328/96 14 01: Safety In.iection Relief Valve Setooint

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Discrepancies. This item was originally discussed in IR 50 327, 328/96-

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14, which documented a November 2, 1996, overpressure condition with the

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Unit 2 safety injection system. A TIA was initiated and after

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completing actions NRR forwarded TIA 97-01 to Region II on April 18,

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1997. The TIA noted that on November 2, 1996, the licensee was not in

compliance with the ANSI code requirements for as found settings of the

subject safety injection system relief valves.

IR 50 327, 328/97 06

identified the issue as VIO 328/97-06 08.

E8.8 (Closed) IFI 327. 328/96 02-02: Review Corrective Actions of PER No.

S0960759PER Recardina CCS Surae Tank Overflow. The inspector reviewed

the above PER and determined that closure for this item was based on

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implementation of NRC commitment NC0960030002. TVA management in a

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realy to a Notice of Violation stated that a design issue will be

su)mitted to address the component cooling system (CCS) surge tank vent

piping arrangement for potential modification of the system.

Based on objective evidence reviewed the inspector verified that Issues

No.96060 and 96061, dated June 13, 1996, were submitted to the Plant

Issues Committee (PIC) by Technical Support in response to the NRC

commitment. The proposed solution for the design deficiency was broader

in scope than the commitment delineated in TVA's letter dated May 22,

1996. The scope of the plant modification for resolution of the design

deficiency will include:

Surge Vent Valve route piping from vent valves 1 FCV 70 66

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to the floor drain located beneath the CCS surge tank.

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Surge Tank level instrumentation replace level transmitter

dry reference leg with a wet reference leg.

The inspector concluded that the corrective action to be implemented by

the proposed plant modification was consistent with the corrective

action delineated in block C.9 of PER No. SQ960759PER and the intent of

the licensee's commitment. This item is closed based on review of

objective evidence.

E8.9 (Closed) IFI 327. 328/93 35 02:

B0P Fuse Control. The inspector

reviewed actions completed by the licensee in connection with

establishing a project to review ar.d upgrade BOP fuse control. TVA

management has taken credit for existing administrative controls of B0P

fuses delineated in procedure SSP 12.2 System and Equipment Status

Control

Revision 20. Additionally, TVA stated that B0P fuses th6t

cause plant transients or power reductions are within the scope of the

Maintenance Rule which requires B0P functional failures to be recorded

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and trended. A root cause analysis is required to be performed and

developed corrective action plans need to be implemented for recurrence

control.

The inspector performed an independent review of SSP-12.2 and verified

that procedural controls have been established for selecting Non 1E

fuses which are installed in circuits identified by the System Operating

Instruction Power Availability List. Procedure SSP 12.2, Section

3.9.1.C identified the Equipment Management System Fuse Tabulation as an

a) proved design output document which is maintained current to reflect

t1e as built plant configuration.

Substitution of Non 1E fuses is

permitted by NE design standard DS E8.1.1 and DS E8.1.2.

This process

is implemented by use of the Non 1E Fuse Substitution List sheen on TVA

drawing 45A700 series and the Non 1E Substitution Notification

Form, Appendix G to SSP 12.2.

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The licensee also stated that a review of Tracking and Reporting of Open

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Items (TROI) for fuse related problems revealed that fuse problems at

Sequoyah are primarily misluling and misidentification.

Fuse size and

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type discrepancies identifieu in B0P circuits have not caused plant

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transients nor plant reliability problems. The inspector reviewed a

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printout of TROI dated May 5, 1997, which had been prepared based on the

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word search fuse. The total listing of plant 3roblems related to the

word " fuse" covered a field of 198 entries. T1e inspector determined

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from this review that objective evidence did not demonstrate that plant

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problems caused by BOP fuses had resulted in plant transients nor

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challenges to safety systems. The inspector concluded that reasonable

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assurance existed for control of B0P fuses. This item is closed based

on the review of objective evidence.

E8.10 (Closed) Unresolved Item (URI) 327. 328/93 02-04:

NRC Review and

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Evaluate GDC 17 Plant Grid Interface.

PER No. SQ940164PER dated March

1, 1994, documented an event where on March 18, 1994, the system peak

load of 24,723 megawatts (MW) exceeded the value of 24,000 MW analyzed

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by the Customer Grou) and resulted in the delayed offset power being

inoperable.

Sequoyal received no notification of this condition and

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compensatory actions required by LC0 3.8.1.1 were never taken.

PER No.

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SQ951121PER dated August 10, 1995, documented an event where on

August 10, 1995, the Transmission and Power Supply (TPS) load

coordinators forecasted a system record peak load of 26,100 MW to occur

on August 14, 1995. The TPS analysis section had set a system load of

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25,722 MW as the maximum analyzed system load for maintaining minimum

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161 kV voltage requirements for Sequoyah offsite power. TPS recommended

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that Sequoyah enter applicable LC0 when the system peak load exceeded

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25,722 MW.

Sequoyah procedure SWYD letter 18, however, had not

established requirements for responding to this scenario. The root

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cause for this deficiency was determined to be ineffective corrective

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action for a previously identified problem. This deficiency was

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corrected by revising procedure Switchyard letter-18, SWYD-18.

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The NRC staff's concern regarding the reliability of the offsite power

grid at Sequoyah were discussed in NRC IR 50-327, 328/93 02 and in a

letter dated March 27, 1996, to TVA recuesting additional information.

TVA's response to that letter was datec July 17, 1996. The NRC has

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reviewed the response received from TVA in connection with this request.

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The staff has, however, determined that additional information is

needed.

In a letter dated January 17, 1997, the NRC requested

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additional information within 60 days of TVA's receipt of the letter.

TVA, in a letter to the NRC dated June 2, 1997, Subject:

Sequoyah

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Nuclear Plant- Response to Request for Additional Information Regarding

Reliability of Offsite Power System (TAC Nos. M93319 and M93320),

provided the information requested. The inspector discussed the

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submittal with TVA's engineering personnel and requested copies of the

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following documents'which provided the basis for TVA's argument

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concerning the adequacy and reliability of the offsite power system:

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DNE Calculation No. SQN GRID STUDY 004 Sequoyah Nuclear

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Plant (SQN) Transmission System Study (TSS) Grid Voltage

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Study of Sequoyah Offsite Power System, Revision 0

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DNE Calculation No. SON GRID-STUDY 003, Transmission System

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Study (TSS) Sequoyah Nuclear Plant (SQN) 161 and 500 kV Grid

Voltage Schedules and Operating Instructions with a

Coincident Extreme Load Forecast Update, Revision 0.

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Switchyard Operations SWYD 18. Plant Voltage Schedule

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Procedure, Revision 15,

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The inspector determined that calculation No. SQN GRID STUDY 004 was a

" Planning" TSS performed on a three year cycle to evaluate steady state

and transient conditions at Sequoyah.

It evaluated the current year

when issued and a five year look ahead. This calculation documented

load flow and transient stability studies of the offsite power system,

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The load flow study determined the minimum acceptable steady state

voltage at Sequoyah to be 153 kV. The study concluded that with an

instantaneous net system load of 28,284 MW: all switchyard inter ties

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closed; and with the Sequoyah capacitor bank in service this design

criteria would be satisfied until the year 2000. The minimum voltage

requirement would be violated in the summer of 2000, under the following

conditions, the Raccoon Mountain inter-tie being out of service is a

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pre event: there is a LOCA for Sequoyah Unit 2: and the Sequoyah inter-

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tie transformer is out of service.

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The transient stability study concluded that there were no voltage

recovery problems on the Unit and shutdown boards.

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Calculation No. SON-GRID STUDY 003 was described as an " operational" TSS

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which is performed on an annual basis.

It defines for the current year

the following:

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The 161 kV and 500 kV operating voltage schedule

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Sequoyah operating parameters for (1) the main generators.

(2) the 500/161 kV inter tie transformer, (3) the 161 kV

capacitor bank

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This calculation used an instantaneous net system peak load of 28,797 MW

and was performed for the following four base cases with various pre-

existing conditions:

1)

All switchyard ties closed

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2)

Sequoyah inter-tie transformer bank outage

3)

Raccoon Mountain inter tie transformer bank outage

4)

Sequoyah inter-tie transformer bank outage and outage of

Sequoyah 161 kV capacitor banks

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The study concluded that the Sequoyah offsite power supply was adequate

for a net system load u) to 28,797 MW with two immediate sources

whenever the capacitor aanks were available. Requirements for ensuring

the availability of the two immediate sources were identified as:

1)

Only if operation of the capacitors includes maintaining

them in automatic control on the wide band continuously.

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2)

And only if specific indicators are monitored and

controlled. These indicators are Sequoyah Unit 2 reactive

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output. Sequoyah 161 kV bus voltage, and Sequoyah 500/161 kV

inter tie transformer bank reactive flow.

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Attachment V of calculation SQN GRID-STUDY 003, Operating Guide

Memorandum, was reviewed and verified to provide new Sequoyah grid

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operating instructions based on the results of the calculation. The

inspector reviewed procedure SWYD-18, Revision 15, and A)pendix C, Units

1 and 2 Gross Reactive Generation Limits, and verified t1at

administrative controls had been established for monitoring and

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controlling the indicators identified above. Section 3.1, Peak System

Load, requires Secuoyah to enter LC0 3.8.1.1 Action d, if the total

system load exceecs those requirements specified in the Chickamauga Load

Dispatcher grid voltage limits which were summarized by Appendix C.

This item is closed based on review of objective evidence and

discussions with NRR concerning the results of the review. Ongoing NRR

review of the issue continues under TAC M93319 and M93320.

E8.11 Ellis and Watts Procurement Activities

NRC's memorandum from Robert M. Gallo, Chief Special Ins)ection Branch

to Johns Jaudon, Director Division of Reactor Safety, Su) ject:

Deficiencies Regarding Air Conditioning Equipment Purchased By the TVA

and Texas Utilities Company from Ellis and Watts, recommended regional

followup of TVA's procurement activities involving Ellis and Watts.

The inspector discussed this issue with TVA's personnel and reviewed

documentation summarizing the results of TVA's Vendor audits of Ellis

and Watts. The licensee has conducted several audits of Ellis and Watts

beginning in September 1976 and continuing up to June 1996.

In February of 1995 based on an action item from PER No. BFPER940133 the

Vendor Audit Services performed an audit to investigate the cause of

problems with TVA/Bechtel Contract 21042-M 01060.

Based on the results

of this audit a restriction was added that all design for assemblies and

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dedication packages for dedicated commercial items be submitted for Site

Engineering ap,roval.

In October of 1995 TVA performed a review of

NUPIC Audit 964-11 and additional restrictions were added concerning

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material verification and traceable weld material. NUPIC recommended

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that utilities have Ellis and Watts submit dedication plans for

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approval. The Vendor Audit Services received information from NUPIC in

April of 1996 that a followup visit to Ellis and Watts revealed

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continuing weaknesses in the driic3 tion process. Based on this

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information Ellis and Watts was dropped from TVA's accepted supplier

list.

E8.12 (Closed) URI 50-327. 328/95 01 01: Caoabilities of Motors to Achieve

Toraue Switch Trio at Dearaded Voltaae and Accident Temoerature. The

licensee had derated the capabilities of actuators with alternating

current motors in accordance with recent information from the actuator

manufacturer on the effects of temperature calculated to be present at

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the time of MOV operation.

NRC Ins 3ection 50 327, 328/95 01 identified

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that the licensee had not ensured tlat the recalculated actuator

capabilities were above the present torcue switch settings.

In the

current inspection, the inspectors founc that the licensee had

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subsequently compared the settings and capabilities and determined that

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the settings of six MOVs should be lowered. The inspectors verified

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that the settings of these MOVs had been appropriately reduced in

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accordance with DCN M10824 during the Cycle 7 refueling outage.

E8.13 (Closed) IFI 50 327. 328/93 36 01: Review of Electrical Modifications

for ERCW MOVs.

This item was opened to provide an NRC review of

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completed modifications to 24 emergency raw cooling water valves. These

were plug valves whose function was to close for containment isolation.

The modification involved changing the valves from torque switch

controlled seating to limit switch controlled seating. The inspectors

verified documentation of adequate comaletion of this modification.

Their review included the PER No. SQPE1930302 that specified the

modification, DCNs M 0937 A and M 09956 A, and examples of a completed

WO (95 00911 00 for valve 1 FCV 67130) and diagnostic post modification

test (for valve 2 FCV 67 139) for the valves.

E8.15 (Closed VIO 01012/EA 95 252:

Failure to Ensure that Provisions of

10 CFR 50.7 were complied with. This violation identified that in July

through September 1991, the licensee discriminated against an employee

engaged in protected activities.

Specific corrective action for this violation was reviewed and

documented in NRC Inspection Report 50-327,328/96 17. This violation is

closed for record purposes; however, the staff will continue to monitor

plant specific indicators related to discriminatory employment

practices. These indicators include, in part, allegations of

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discrimination reported to the NRC and proceedings initiated as a result

of complaints made to the Department of Labor alleging discrimination

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for engaging in protected activity.

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IV. P1 ant Support

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Radiological Protection and Chemistry (RP&C) Controls (71750, 83750,

84750, 86750, TI 2515/133)

R1.2 Transoortation of Radioactive Materials

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a.

Insoection Scope

The inspctors evaluated the licensee's transprtation of radioactive

materials program for implementing the revised Department of

Transportation (D0T) and NRC trans>ortation regulations for shipment of

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radioactive materials as required )y 10 CFR 71.5 and 49 CFR Parts 100

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through 177.

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b.

Observations and Findinas

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The inspectors reviewed procedures and determined that they adequately

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addressed the following:

1) assuring that the receiver has a license to

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receive the material being shipped: 2) assigning the form, quantity

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type, and proper shipping name of the material to be shipped: 3)

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classifying waste destined for burial: 4) selecting the type of package

required: 5) assuring that the radiation and contamination limits were

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met; and 6) preparing shipping papers.

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The licensee's records for technical staff training were reviewed and

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the inspectors determined that the technical staff had received the

requisite training for rad material shipments. The training for the

technical staff this year has been scheduled for July.

The inspectors requested that the licensee produce a sample shipping

manifest using their software program. The inspectors provided sample

input information and the resultant printed sample manifest was

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reviewed. The inspectors determined that the form met the current

requirements.

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c.

Conclusions

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Based on the above reviews, the inspectors determined that the licensee

had effectively implemented a program for shipping radioactive materials

required by NRC and D0T regulations.

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R1.3 Occuoational Radiation Exoosure Control Proaram

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a.

Insoection Scope

The inspectors reviewed implementation of selected elements of the

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licensee's radiation protection program (10 CFR 20.1101). The review

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included observation of radiological protection activities including

personnel monitoring (10 CFR 20.1502), radiological postings

(10 CFR 20.1904 & 1902), high radiation area controls (10 CFR 20.1601 &

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1602), and verification of posted radiation dose rates (10 CFR 20.1501 &

1502) and contamination controls within the RCA. The inspectors also

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reviewed licensee records of personnel radiation exposure and discussed

as low as reasonably achievable (ALARA) program details, implementation,

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and goals.

b.

Observations and Findinas

The inspectors toured Auxiliary Building facilities, Truck Bay, and

radioactive waste storage area. At the time of the inspection,

radiological housekeeping was observed to be good. Radiologically

controlled areas observed were appropriately posted and radioactive

material observed was appropriately stored and labeled.

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The inspectors reviewed the postings and performed independent

contamination and boundary radiation surveys in the auxiliary building

at the boric acid pumps and storage tanks. All postings were found

accurate and current.

Boundary surveys were as posted and no

contamination was found on the inspector requested smears.

The Fiscal Year 1997 site exposure goal has been set at 300 person rem.

At the time of the inspection, the site person-rem was about 275.105

Jerson rem (not TLD corrected); thus, about 92 percent of the goal had

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3een expended. Individual radiation worker internal and external doses

were being maintained well below regulatory limits and the licensee was

continuing to maintain exposures ALARA.

The inspectors reviewed PER No. SQ970929PER and the actions taken by tfe

licensee in response to the identified problem. On A)ril 8, 1997 a

Radiography supervisor did not comply with Procedure ,1CI 16 " Radiation

Protection During Radiographic Operations" Revision 3, and Procedure

RCI-14 " Radiation Work Permit (RWP) Program" Revision 20. Specifically,

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the Radiograahy supervisor did not: (1) receive authorization from the

responsible ladcon Shift Supervisor prior to exposing the source (RCI 16

Step 7.7E) (2) positively verify personnel were evacuated from the

established zone prior to exposing the source (RCI 16 Step 7.7A) and (3)

follow the conditions required by the RWP (RCI-14 Step 7.1).

The

licensee immediately stopped radiography operations. The event was

reviewed and written statements from personnel who were present were

discussed during a meeting with affected employees. TLD and electronic

dosimetry results were analyzed and no measurable dose was found. This

was primarily due to distance from the source, worker location and the

short source exposure.

Exposure to the affected radiography area had

been controlled by the radiographer in compliance with his safety

manual. The licensee instituted the following interim corrective

actions: (1) Adequacy of communications was stressed (2) The effects of

fatigue were reviewed (3) Radiography RWP's to be written and approved

by the Radeon Manager, and (4) Radcon personnel were briefed on

responsibilities and expectations for Radiographic Operations. The

licensee made a informational call to Region II and the notified the

Site Resident Office. The licensee was informed that the failure to

follow licensee site procedures was a violation. This licensee-

.-

. . -

.

.

. .

,

.

.

I

51

identified and corrected violation is being treated as a Non Cited

Violation consistent with Section IV of the NRC Enforcement Policy. (NCV

'

50-327, 328/97-06-10).

The inspectors reviewed PER No. SQ971429PER that involved a spill of

radioactive liquid at ap

elevation Railroad Bay. proximately 16:25 on May 19,1997, in the 706'

The liquid came from a failed conductivity

arobe on the inlet to the Modularized Fluidized Transfer

Jemineralization System (MFTDS). Approximately 3000 gallons were

"

released during the spill and about 300 gallons were released from the

Waste Packaging Area to the rad waste yard immediately adjacent to the

railroad Bay Door. The inspectors reviewed Procedure 0 VI 0PS 077 001.0

" Operating Procedure for CNSI Modular Fluidized Transfer

Demineralization System

Chem Nuclear Systems, INC", Revision 1.

At

the time of the inspection decontamination had been completed inside of

,

the plant and the areas had been released. The inspectors reviewed the

,

clean up activities and the results of the soil samples from the

excavated soil. Approximately 4500 cubic feet of slightly contaminated

soil and asphalt paving had been removed and the process of backfilling

the excavation was underway. Samples of the storm drain in the

proximity to the rad waste yard indicated no presence of the spilled

material. The yard pond was also sampled and indicated no presence of

contamination. There were no personnel contaminations or injuries as a

.

result of the spill. Closeout activities from the spill were still in

progress.

Preliminary dose estimates by the licensee using conservative

assumptions (upper bounding dose) determined the incremental maximum

individual dose at the site boundary (0.870 km in the South Direction)

to be 2.75 E 04 mrem to the Liver (critical organ) and 1.40 E 04 mrem to

the total body. These doses are small percentages of annual dose

limits. The inspectors reviewed the Action Plan for Recovering EL 706'

Radwaste Yard, Revision 1 dated June 25, 1997.

During a. followup tour

,

of the Railroad Bay the ins sectors noticed physical openings alongside

-

of the railroad tracks whic1 pass under the door. An empirical

4

measurement of air flow performed by the inspectors found that the flow

was toward the outside. Review of the Updated Final Safety Analysis

'

Report at Section 9.4.2.1 Design Ba~is for the Auxiliary Building states

that " Areas of the building which ar. subject to radioactive

contamination are maintained at a slig:? negative pressure to limit out

leakage.

In addition, the system has the cap:bility of isolating the

'

contaminated areas from outdoors. All exhaust ah is routed through a

duct system, and is discharged into the Auxiliary BLilding exhaust stack

which is located atop the Auxiliary Building, and extends above the

roof." In addition Detailed Design Criteria WO. SQN DC V 1.1.7 Titled

Auxiliary Building Railroad Access Door ead Associated Equipment, dated

July 29, 1971, states in Section 3.3, Falure Criteria, "During normal

!

conditions with a pressure differentia; of 1/4" water, air leakage for

the door is not to exceed 1500 cfm". Section 4.1.2. Seals, states

" Removable, rubber blocks shall be pr(vided for sealing at each of the

railroad rails where they pass f "ough the embedded door sill". A

i

search of the Work Request SysN idencified a work request No: C053504

dated April 14, 1994 associatid with the Roll up Door. The request

,

identified the rubber seals in the railroad tracks as having

,

.

,

',

52

deteriorated and needing replacement. At the time of the ins

seals had not been replaced although the WR was still active.pection the

The

failure to replace the rubber gasket seals and the failure to maintain

the auxiliary building at a negative pressure at this location were

identified as a violation (50 327, 328/97-0611).

c.

Conclusions

Radiological facility controls and housekeeping in radioactive waste

storage areas were obrerved to be good. Material was labeled

appropriately, and areas were pro)erly posted.

Radiation worker

internal and external doses were )eing maintained well below regulatory

limits and the licensee was continuing to maintain exposures ALARA. One

non cited and one cited violation were identified.

>

R1.4 Water Chemistry Controls

a.

Inspection Scoce

The inspectors reviewed implementation of selected elements of the

licensee's water chemistry control program for monitoring primary and

secondary water quality. The review included examination of program

guidance and implementing procedures and analytical results for selected

chemistry parameters,

b.

Observations and Findinas

The inspectors reviewed technical specifications (TSs), which described

the operational and surveillance requirements for reactor coolant

activity and chemistry, and Final Safety Analysis Report (FSAR), Section

10.3.5, Water Chemistry. The section indicated that guidelines for

maintaining reactor coolant and feedwater quality were derived from

vendor recommendations and the current revisions of the Electric Power

Research Institute (EPRI) Pressurized Water Reactor (PWR) Primary and

Secondary Water Chemistry Guidelines. The UFSAR also indicated that

detailed operating specifications for the chemistry of those systems

were addressed in the Station Chemistry Section.

The inspectors reviewed selected analytical results recorded for Unit 1

and Unit 2 reactor coolant and secondary samples taken during the

inspection period. The selected parameters reviewed for primary

chemistry included dissolved oxygen, chloride, fluoride, and sulfate

levels. The selected parameters reviewed for secondary chemistry

included hydrazine, iron, and cop>er levels. Those primary parameters

reviewed were maintained well wit 11n the relevant TSs limits and within

the EPRI guidelines for power operations.

The ins)ectors reviewed the June 16, 1997 memo from reactor engineering

to the )lant Manager discussing Sequoyah Units 1 and 2 Fuel Integrity

Status. Unit 1 observed an instantaneous fuel defect event after about

8 Effective Fuel Power Days burnup, May 23, 1997, after starting Cycle 9

defect free.

Indications were that 2-3 " average" defects occurred.

_

.

.

_

_

_.

. .

\\

.

.

53

.

Unit I was classified in Action 1 of Site Standard Practice (SSP) SSP-

)

i

12.55 Fuel Integrity Assessment Program.

Unit 2 continues in Action 1.

1

.

One defect was believed to have been carried over from Cycle 7 and the

{

licensee believes the defect has a high probability of discharge during

-

the next outage. The conditions that define Action 1 are: 0.003 < I-

131 s 0.025 C1/g or 0.1 s Xe-133 s 1.0 pC1/g. The actions ::pecified

are: (1) Notify plant management and Nuclear Fuel (2) Estimate number,

nature, and burnup of failed fuel (3) Determine possible causes and

appropriate actions to mitigate radiological impact and prevent

'

additional failures (4) Survey industry experience (5) Notify fuel

supplier (6) Establish contingencies for fuel inspection. The

inspectors reviewed the isotopic results and confirmed that the actions

taken were as stated in the SSP.

c.

Conclusions

Based on the above reviews, it was concluded that the licensee's water

chemistry control program for monitoring primary and secondary water

quality had been implemented, for those )arameters reviewed, in

accordance with the TSs requirements. T1e Fuel Integrity Assessment

team was aerforming the required fuel integrity assessments as specified

by the SS).

'

R1.5 Annual Effluent Release Report and Annual Radiolooical Environmental

Operatina Report

a.

Insoection Scope

Technical Specifications Section 6.8.1(1) titled Offsite Dose

Calculation Manual details the methodology and parameters used in the

calculation of offsite doses.

Section 5.1 and 5.2 require the

submission of The 1996 Annual Radioactive Effluent Release Report and

Annual Radioloaical Environmental Ooeratina Report,

b.

Observations and Findinas

The inspectors reviewed The 1996 Annual Radioactive Effluent Release

Report. The report detailed the solid waste shipped offsite for burial

or disposition. A tabulation for this waste is listed below.

.

..

'.

54

Type of Waste

Unit

12 Month

Est. Tot.

Period

Error %

i

a.

Spent resins, filter

m'

2.19E+01

i5.00E 01

sludges, evaporator

Ci

5.65E+02

i1.50E+00

i

bottoms, etc.

b.

Dry Active Waste,

m'

5.75E+01

i5.00E 01

Compressible Waste

Ci

7.43E+00

i5.00E 01

Contaminated Equipment,

etc.

c.

Irradiated Components,

m'

None

N/A

Control

Ci

None

N/A

Rods, etc.

d.

Other - Thermal destruction

m'

6.06E+00

i5.00E 01

of scintillation fluids

Ci

3.35E+01

i5.00E 01

'

External gamma radiation levels were measured by thermoluminescent

dosimeters (TLDs) deployed around Sequoyah as part of the offsite

Environmental Radiological Monitoring Program. The quarterly gamma

radiation levels determined from these TLDs during this reporting period

averaged approximately 15.7 mR/ quarter at onsite (at or near the site

boundary) stations and approximately 14.5 mR/ quarter at offsite stations or

approximately 1.2 mR/ quarter higher onsite than at offsite stations. This

may be attributable to natural variations in environmental radiation

levels, earth moving activities onsite, the mass of concrete employed in

j

the construction of the plants, or other undetermined influences.

Fluctuations in natural background dose rates and in TLD readings tend to

mask any small increments which may be due to plant operations.

Sequoyah

Environmental TLD Direct Radiation Environmental Monitoring results

reported for the first quarter 1997 in NUREG-0837 NRC TLD Direct Radiation

Konitorina Network range from 16.5 t 0.9 mR/Std.Qtr to 17.1 i 1.6 mR/Std.

Otr.. There were no aty)ical results for Sequoyah identified in the NUREG.

The licensee concluded t1at there was no identifiable increase in dose rate

levels attributable to direct radiation from plant equipment and/or gaseous

effluents.

,

To determine compliance with 40 CFR 190, annual total dose contribution to

the maximum individual from Sequoyah radioactive effluents and all other

nearby uranium fuel cycle sources were considered. Cumulative annual total

doses are presented in the following table.

.

I

-

_ - .

- _.

_-

-

_ - .

-

--

.

.-

-

-.

.

,

'

. .

'

.

'

55

.

Total Dose from Fuel Cycle

1996

1

.

'

First

Second

Third

Fourth

Dese

Quarter

Quarter

Quarter

Quarter

i

Total Body or any Organ (except thyroid)

Total body air

7.88E 04

1.05E 03

8.22E 04

1.39E-03

submersion

Critical organ dose

1.04E 02

7.74E 03

1.90E 02

1.84E-02

(air)

l

Total body dose

1.7E-02

1.9E 02

5.6E 03

2.1E 03

'

(liquid)

,

Maximum organ dose

2.3E 02

2.5E 02

7.1E 03

2.5E 03

'

-

(liquid)

Direct Radiation Dose

0.0E 00

0.0E 00

0.0E 00

0.0E-00

Total

5.1E-02

5.3E-02

3.3E-02

2.4E-02

Cumulative Total Dose (aren)

1.6E-01

'

Annual Dose Limit (ares)

2.50E401

Percent of Limit

<12

5

Thyroid

1

Total body air

7.88E 04

1.05E 03

8.22E 04

1.39E 03

submersion

Thyroid dose

1.04E 02

7.74E 03

1.90E-02

1.85E 02

(airborne)

1

Total body dose

1.7E 02

1.9E-02

5.6E 03

2.1E 03

(liquid)

Thyroid dose (liquid)

3.2E-03

4.5E 03

2.1E 03

1.7E 03

)

Direct Radiation Dose

0.0E-00

0.0E 00

0.0E 00

0.0E 00

Total

3.1E-02

3.2E-02

2.8E-02

2.4E-02

Cumulative Total Dose (ares)

1.2E-01

Annual Dose Limit (ares)

7.50E+01

Percent of Limit

<1%

l

The inspectors selectively reviewed the Annual Radioloaical

Environmental Ooeratina Report and the data supporting the report. The

inspectors' review of the data determined that there was no

radioactivity attributable to the plant detected in the 1996 monitoring

program.

Environmental radioactivity measured by the program was due to

naturally occurring radioactive materials or radionuclides commonly

found in the environment as a result of atmospheric fallout. The

exposures calculated from the Annual Radioloaical Environmental

Doeratina Report resultant data were consistent with results from the

preoperational monitoring program.

- .

.-.

--

-

-

.

.

'

. .

i

.

'

56

c.

Conclusions

The radiological imaact from the facility operation was less than 1

percent of the 40 C R 190 regulatory limit. The exposures calculated

from the 1996 Annual Radioactive Effluent Release Report resultant data

)

were consistent with results from the preoperational monitoring program.

V. Manaaement Meetinos

,

X1

Exit Meeting Summary

The inspectors ) resented the inspection results to members of licensee

management at t1e conclusion of the inspection on July 16, 1997. The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials would be

<

considered proprietary.

No proprietary information was identified.

PARTIAL LIST OF PERSONS CONTACTED

Licensee

~

  • Bajestani, M., Site Vice President (as of June 30, 1997)
  • Beasley, J., Acting Site Quality Manager

Bryant, L., Outage Manager

  • Burton, C.. Engineering and Support Services Manager
  • Butterworth, H., Operations Manager
  • Flippo

T., Site Support Manager

-

Herron,

J., Plant Manager

Hunt, W., Operations Training Manager

Kent, C., Radcon/ Chemistry Manager

  • Koehl, D, Assistant Plant Manager
  • Lorek, M., System Engineering Manager

O' Brian, B., Maintenance Manager

Reynolds, J., Operations Superintendent

  • Rupert, J., Engineering and Support Services Manager
  • Salas, P., Manager of Licensing and Industry Affairs
  • Valente,

J., Engineering & Materials Manager

  • Attended exit interview

.

INSPECTION PROCEDURES USED

,

IP 37550:

Engineering

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls In Identifying,

<

Resolving, & Preventing Problems

IP 61700:

Surveillance Procedures and Records

.

.

..

. . .

. .

'

.

57

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

-

IP 64704:

Fire Protection Program

IP 71707:

Plant Oprations

IP 71714:

Cold Weather Preparations

IP 71750:

Plant Support Activities

IP 83750:

Occupational Radiation Exposure

IP 84750:

Radioactive Waste Treatment, And Effluent And Environmental

.

Monitoring

IP 86750:

Solid Radioactive Waste Management And Transportation Of

Radioactive Materials

IP 92901:

Followup - Operations

-

IP 92902:

Followup

Maintenance

IP 92903:

Followup

Engineering

TI 2515/109:

Inspection Requirements for Generic Letter 89 10,

Safety Related Motor 0perated Valve Testing and

Surveillance

TI 2515/133:

Implementation of Revised 49 CFR 100179 and 10 CFR 71

4

ITEMS OPENED. CLOSED. AND DISCUSSED

'

--

The following escalated enforcement items (EEI) were reviewed as part of an

enforcement conference with the licensee on June 27, 1997. Subsequent

,

enforcement was taken on the issues by letter dated July 10, 1997.

Based on

the enforcement conference and two violations issued on July 10, 1997, the

EEIs listed below are closed.

Followup of licensee corrective actions for the

violations documented in the July 10, 1997, enforcement action will be

conducted as part of the violation closecuts.

Tyge Item Number

Status

Description and Reference

_

EEI

50-327, 328/97 05 01

Closed

Inadequate Corrective Actions for

EA 97 232

the 1993 Drain Down Event

.

EEI

50 327, 328/97 05 02

Closed

Failure to Follow SSP 12.1, Conduct

EA 97-232

Operations

,

The following violations were issued as a result of escalated enforcement

action taken on July 10, 1997.

,

Tvoe Item Number

Status

Description and Reference

VIO

01013

Open

Failure to Identify and Take

>

EA 97-232

Corrective Actions for Loss of RCS

Inventory Cont ml While Draining

Pressurizer (IR 50 327, 328/97 05)

.

-

.-

.

-

-

.. - .-

_

-

.-

'

c

.

.

,

o

58

VIO

01023

Open

Failure Properly Log a Unit 1

,

EA 97 232

RCS Drain Down Evolution (IR 50 327.

-

328/97-05)

-

Ooened

Type Item Number

Status

Descriotion and Reference

_

NCV

50 328/97-06 01

Ogn/

Failure to Follow Procedure Which

i

Close

Resulted in Establishing a Flow Path

'

for ERCW to Enter and Contaminate

the "A" CST (Section 01.3)

-

IFI

50 327, 328/97 06-03

Open

Review the Licensee *s Emergency

'

Diesel Generator Reliability and

Failure Analysis (Section M1.2)

NCV

50-327/97 06 04

Open/

Failure to Inspect Both Sides of

Closed

Nine Fire Barrier Penetration Seals

as Required by Procedures (Section

M1.4)

NCV

50 328/97 06 05

Ogn/

Failure to Follow a Maintenance Work

Close

Order Resulting in Work on Wrong

'

Valve (Section M4.1)

'

NCV

50-327, 328/97 06 06

Open/

Failure to Properly Perform

Close

Surveillance Testing (Section M4.2)

IFI

50 327, 328/97 06 07

Open

Actions to Resolve Remaining GL 89-

10 Issues (Section E1.1)

VIO

50 328/97 06-08

Open

Inadequate Corrective Actions for

,

Deficient Safety Injection System

Relief Valves Lifting Setpoints

(Section E2.1)

URI

50 327/97 06-09

Open

Remote Position Indication Testing

(Section E2.2)

NCV

50 327, 328/97 06-10

Open/

Failure to Follow Procedures RCI-14

Closed

and RCI 16 (Section R1.3)

VIO

50 327, 328/97 06 11

Open

Failure to Meet 10 CFR 50, Appendix

B, Criterion XVI, Corrective Action,

Requiring That Measures Shall be

Established to Assure that

Conditions Adverse to Quality are

Promptly Identified and Corrected

(Section R1.3)

.

.

.-

..

_

. . .

_ _ _

...

'

..

'

.

59

Closed

Tygg Item Number

Status

Description and Reference

_

LER

50 328/96 007

Closed

Engineered Safety Feature (ESF)

Actuation, Start of the Auxiliary

Feedwater System, As a Result of

Inadequate Return of Equipment to

Service (Section 08.1)

.

LER

50 327/96 006

Closed

A Failed Coupled Capacitor Potential

Device Caused Actuation of the

Generator Backup / Transformer Feeder

Relay Tripping the Turbine and the

Reactor (Section 08.2)

IFI

50-328/97 01 05

Closed

Review Root Cause Which Led to N0ED

!

on EDG (Section 08.3)

LER

50 327/97 002

Closed

Enforcement Discretion Granted When

Problems With the 2A A Diesel

Generator Actuator Was Identified

(Section 08.3)

i

VIO

50 327, 328/96-02 05

Closed

Failure to Control Implementation of

Plant Modifications as Required By

SSP-9.3 (Section M8.1)

'

VIO

50 327, 328/96 12 01

Closed

Failure to Revise Emergency

Operating Procedures as a Result of

,

Design Changes to Abandon Plant

Equipment (Section M8.2)

LER

50-328/96 003

Closed

Reactor Trip Breakers Were Manually

Opened With An Automatic Generation

".

of a Feedwater Isolation Signal and

'

a Manual Reactor Trip (Section M8.3)

LER

50 328/96 006

Closed

Automatic Reactor Trip of the Loss

of Power to Start Bus 2A, tho Start

of Four Emergency Diesel Generators,

and Loading of Emergency Diesel

Generator 28 B (Section M8.4)

l

LER

50 327/97 001

Closed

Failure to Properly Perform

Surveillance Testing on the EDG

Timer Relays that are Contained in

the Start Logic Circuity (Section

M8.5)

-

_.

- .

-

-

_.

..

.

.

l

f

60

l

'

LER

50 327/97 003

Closed

Failure to Properly Perform

Surveillance Testing on the

Centrifugal Charging Pump Inlet

Isolation Valve Logic (Section M8.6)

j

l

l

LER

50 327/97 008

Closed

Failure to Properly Perform

Surveillance Testing on the

!

Containment Air Return Fan Start

'

Logic and on the Blackout and Auto

'

Sequencing of the Station Fire Pumps

l

(Section M8.7)

IFI

50-327, 328/94 30-01

Closed

Deficiencies in Check Valve Program

Implementation (Section M8.8)

IFI

50 327, 328/94 30 02

Closed

Inadequate Preventive Maintenance on

,

!

Reach Rod Valves (Section M8.9)

IFI

50 327, 328/94 22 02

Closed

Snubber Design and Maintenance Items

(Section M8.10)

VIO

50 327, 328/97 03 02

Closed

Failure to Follow Instructions in a

Work Order Resulting in an ESF

q

Actuation (Section E8.1)

l

LER

50 327/97 007

Closed

Diesel Generator Starts That

Resulted From Cutting a Cable While

Drilling a Panel and During Re) airs

to the Damaged Cable (Section 18.1)

I

LER

50 327/96 004

Closed

Inadvertent Engineered Safety

Feature (ESF) Actuation, Loss of

Power Signal and Start of Four

,

Diesel Generators (Section E8.2)

LER

50-327/96 008

Closed

A Quarterly Backseat / Closure Test on

F%e Check Valves On Each Unit Was

l

Not Performed As Required By the

l

American Society of Mechanical

l

Engineers (ASME)Section XI In-

l

Service Valve Testing Program Basis

l

Document (Section E8.3)

LER

50 327/96 009

Closed

An Auxiliary Building Secondary

Containment Boundary / Fire Barrier

Was Not Maintained as Required by

Design Resulting From a Failure to

'

Follow the Design Control Process

,

(Section E8.4)

,

-

_ _ . . _ . _ - _ _ _ _ . _ _ _ _ _ _ _ _ . _ _ . _ . _ _

f

-

. .

-

.

61

IFI

50 327, 328/96-14 02

Closed

Review Corrective Actions Related to

Continuing Steam Dump System

Operational Problems (Section E8.5)

IFI

50-327, 328/96-17-03

Closed

Steam Dum) Drain System Improvements

,

l

(Section E8.5)

'

LER

50 328/96 004

Closed

After a Reactor Trip Breaker Was

!

Removed It Was Found To Have

Inoperable Auxiliary Contacts

i

(Section E8.6)

LER

50 328/96 004

Closed

After a Reactor Trip Breaker Was

Revision 01

Removed, It Has Found To Have

l

Inoperable Auxiliary Contacts

,

(Section E8.6)

IFI

328/96 14 01

Closed

Safety Injection Relief Valve

l

Setpoint Discrepancies (Section

l

E8.7)

l

IFI

327, 328/96 02 02

Closed

Review Corrective Actions of PER No.

l

SQ960759PER Regarding CCS Surge Tank

j

Overflow (Section E8.8)

IFI

327, 328/93 35 02

Closed

B0P Fuse Control (Section E8.9)

URI

327, 328/93 02 04

Closed

NRC Review and Evaluate GDC 17 Plant

Grid Interface (Section E8.10)

l

'

URI

50 327, 328/95 01 01

Closed

Capabilities of Motors to Achieve

Torque Switch Trip at Degraded

,

Voltage and Accident Temperature.

l

(Section E8.12)

IFI

50 327, 328/93-36 01

Closed

Review of Electrical Modifications

for ERCW MOVs (Section E8.13)

VIO

01012 EA 95 252

Closed

Failure to Ensure that Provisions of

l

10 CFR 50.7 Were Complied with

!

(Section E8.15)

l

<

l

e

. _ . - .

e

. - . _ - .

. . . . - .

- - - .

~ - - . +

- ~ - - - r- - ~ ~

- - - - - - --- - - ' ~

.

  • O

!

g2 Mo

l

g

j ,

UNITED STATES

NUCLEAR REGULATORY COMMISSION

C

WASHINGTON, D.C. 20666 4 001

%-

May 21, 1997

c

MEMORANDUM T0:

Jon,RJJohkon,iDirector,.._

Division of Reactor Projects

Region II

FROM:

Frederick J. Hebdon, Director C

i

Project Directorate II-3

5#

t

_

-

-

Division of Reactor Projects - I/II

Office of Nuclear Reactor Regulation

SUBJECT:

NRR RESPONSE TO TIA 97-01, SEQUOYAH NUCLEAR PLANT, UNITS 1

AND 2 - RELIEF VALVE LIFT SETTINGS REQUIRED BY APPLICABLE

,

l

CODES (TAC NO. M97281)

.

By memorandum dated January 15, 1997, Region II requested technical assistance

l

regarding the regulatory requirements and acceptance criteria for relief

valves. An issue was raised during plant heatup of Sequoyah Unit 2 in

'

November 1996. During this heatup, the Safety Injection system pump discharge

header was noted to be pressurized to 1850 psig due to check valve back-

l

leakage; the system design pressure is 1750 psig. Although the nominal

i

setpoint for the three relief valves on the header-is also 1750 psig, none of

the relief valves had lifted to relieve pressure. Because of Tennessee Valley

Authority's (TVA's) interpretation of the applicable codes, as discussed in

the Task Interface Agreement request, TVA concluded that failure of the valves

to lift at 1850 psig did not constitute an operability or reportability. issue.

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Region II disagrees with TVA's conclusion and has asked for a NRR position.

NRR has completed its review of this issue and has developed the position in

regards to TVA's code interpretation / practice as noted in the attachment.

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Docket No. 50-327 and 50-328

Attachment:

Evaluation

cc w/ attachment:

R. Cooper, Region I

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W. L. Axelson, Region III

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J. Dyer, Region IV

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Attachment

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RESPONSE TO REGION II TASK INTERFACE AGREEMENT (TIAl 97-01

EVALUATION OF SE000YAH PRACTICE REGARDING RELIEF VALVE SETP0INTS

Description of Event

In a memorandum dated January 15, 1997, Region II requested NRR assistanca

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regarding issues involving the as-found setpoints of plant safety injection

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(SI) system relief valves. During an event at Sequoyah Unit 2 on November 2,

1996, the plant licensee found an SI piping segment, which is isolated from

the primary coolant by check valves, to be pressurized to 1850 psig. The

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nominal setpoints for the system relief valves are 1750 psig (also the system

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design pressure), but the valves apparently did not lift to relieve the

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pressure from apparent back-leakage through the check valves.

The Region has

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provided information from the licensee's relief valve test program and

excerpts from the system design codes- American Society of Mechanical Engineers

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(ASME)Section VIII for vessels and American National Standards Institute

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(ANSI) 831.7 for piping).

The licensee's test procedure involves setting the

relief valves to within

3% of the nominal settings and allows another i 3%

for as-found conditions when the valves are retested after being in service.

Following the event on November 2,1996, one of the three system relief valves

was tested and found to have a setpoint of 1840 psig which is within the

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licensee's high side acceptance criterion of 1750 psig + 3% + 3% (or 1855

psig). The licensee stated that this condition did not require reporting or

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cause the valves to be inoperable.

Specifically, the Region is requesting NRR

assistance regarding the following:

1.

What establishes the regulatory requirements for relief valve setpoints

at Sequoyah?

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2.

What is the maximum allowable as-left condition, including tolerance,

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when setting the relief valves? Should it be set at or below the system

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design pressure of 1750 psig or can it be set at 1750 i 3%?

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3.

Is the condition of the two untested relief valves acceptable, knowing

that they will not lift up to 1850 psig in a system with a de::ign

pressure of 1750 psig? Can the licensee's program have up to 6% drift

from nominal setpoint and still consider the valves to be acceptable?

Evaluation

The NRR Mechanical Engineering Branch has evaluated these issues, and the

results of our review for the above three items are discussed below,

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ATTACHMENT

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1.

The NRR staff agrees with the Region II concern that the licensee's

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relief valve testing procedure and acceptance criteria may not meet all

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requirements.

It is our conclusion that it is improper to stack (or-

add) the as-left and as-found tolerances together to obtain an even

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higher allowable limit. To do so is inconsistent with other

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requirements, is not logical, and is misleading.

For example, no

licensee (including this one) is allowed to take the i 1% as-left

criterion for the pressurizer safety valves or the main steam safety

valves and add it to the i 1% (or i 3%) as-found criterion to obtain

i 2% (or i 4%) to satisfy the plant technical specifications for

operability.

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The as-left tolerance for setting relief valves is allowed to be as high

as i 3% by some design codes including the Section VIII Code applicable

to Sequoyah and the later Section III Codes for some liquid relief

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valves.

(The B31.7 Code for piping does not provide a specific

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allowable as-left tolerance; however, some piping designed to B31.7

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requirements also attaches to a Section VIII or Section III vessel such

that the i 3% would apply.) Also, ASME OM-1 for testing of pressure

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relief devices requires resetting and other actions if setpoints exceed

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3% of their stamped set pressures. As a practical consideration,

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as-left criteria should be based on the capability of the most accurate

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and precise methodology available. .That is, as-left criteria should be

significantly less than as-found criteria since relief valves are known

to drift, and it is not desired to exceed the as-found criteria when the

valves are next tested after some time in service.

Therefore, a more

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stringent as-left tolerance should be favorable for helping assure

setpoints within the as-found tolerance.

The as-found tolerance should be supported by an analysis of the

limiting operational or transient events for overpressure or other

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safety parameters to verify that the design limits of the piping,

vessel, or system are not exceeded. Apparently, the as-found setpoint

tolerance for the SI system relief valves which has been used at

Sequoyah is effectively i 6%; however, it is not clear that the licensee

clearly defines that the relief valves are allowed to drift this much

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and that the licensee has an analysis which demonstrates that i 6% is

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acceptable.

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2.

In order to meet ASME or ANSI Code requirements, certain system relief

valves are required to be set at pressures no higher than the system

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design pressures.

It is our conclusion that the highest as-left

setpoints are allowed to be based on adding the nominal setpoint values

and the as-left tolerance criteria when setting the setpoints, assuming

a supporting analysis exists.

For example, if a relief valve has a

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nominal setpoint of 1750 psig and a i 3% as-left tolerance, the valves

could be set at 1750 psig + 3% (or 1803 psig), even though 1750 psig is

the system design pressure.

This is consistent with the ASME Code since

the Code does not require that valves be set with zero tolerance, and

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the supporting analysis must include the effects of the allowed as-found

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setpoint tolerance.

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3.

Because of the considerations in item 1 above, NRR concludes that the

licensee's procedure for testing the one relief valve may be inadequate

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if the procedure does not clearly indicate what the as-found setpoint

criteria is or if the licensee has no analysis which demonstrates that

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the as-found criteria is acceptable. The as-found tolerance should be a

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clearly identified number or percentage. range (i.e., not the result of

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adding two tolerances together), and the supporting analysis should

demonstrate that the peak overpressure and other limiting safety

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parameters are acceptable. Therefore, if the licensee has not

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demonstrated that i 6% is the acceptable as-found setpoint tolerance,

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the operability of the other two SI system relief valves would be in

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question.

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