ML20134G048
| ML20134G048 | |
| Person / Time | |
|---|---|
| Site: | Zion File:ZionSolutions icon.png |
| Issue date: | 01/28/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III) |
| To: | |
| Shared Package | |
| ML20134G033 | List: |
| References | |
| 50-295-96-14, 50-304-96-14, NUDOCS 9702100257 | |
| Download: ML20134G048 (29) | |
See also: IR 05000295/1996014
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U.S. NUCLEAR REGULATORY COMMISSION
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REGION III
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Docket Nos:
50-295. 50-304
License Nos:
Report No:
50-295/960014, 50-304/960014
Licensee:
Commonwealth Edison Company
Facility:
Zion Nuclear Plant, Units 1 and 2
Location:
Opus West III
1400 Opus West III
Downers Grove IL 60515
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Dates:
August 24 - October 11, 1996
Inspectors:
R. A. Westberg, Acting Senior Resident
Inspector
D. R. Calhoun. Resident Inspector
D. M. Chyu. Resident Inspector
E. W. Cobey, Resident Inspector
D. E. Jones, Reactor Engineer
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D. W. Rich, Reactor Engineer
Approved by:
Marc L. Dapas, Chief
Reactor Projects Branch 2
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9702100257 970128
ADOCK 05000295
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EXECUTIVE SUMMARY
Zion Nuclear Plant. Units 1 and 2
NRC Inspection Reports 50-295/96 14: 50-304/96-14
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This inspection included aspects of licensee operations, maintenance, and
engineering.
The report covers a seven-week period of inspection activities
by the resident staff and regional projects inspectors.
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Operational Jerformance was characterized by frequent operational events,
several of w1ich resulted in inadvertent limiting conditions for operation
(LCO) entries. The licensee was ineffective in averting the previously
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identified trend in personnel errors.
Furthermore, several procedures were
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00erations
An inadvertent isolation of component cooling water flow to the 2B
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safety injection pump and resultant LCO entry was caused by inadequate
equipment attendant (EA) communications and understanding of duties.
This event also resulted in a violation for the failure to follow
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procedures governing work controls (Section 01.1).
The inspectors identified a violation involving multiple failures to
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stop withdrawing control rods and enter the appropriate abnormal
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operating procedure upon indications of rod misalignment. This event
manifested deficiencies in communication of expectations for ccaduct of
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startup, in command and control during rod withdrawal, and in operator
sensitivity to possible rod misalignment due to known position
indication problems (Section 01.2).
The inspectors identified a violation in which, due to an incorrect
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understanding of Technical Specifications (TS), the licensee did not
complete TS action requirements for inoperable emergency diesel
generators (EDGs) within the required time frame on several occasions
(Section 01.3).
A demineralized water spill in the Unit 2 containment Tesulted from a
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failure of a general operating procedure to provide sufficient plant
configuration controls (Section 01.4).
The failure to properly unload EDGs upon completing surveillance tests
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due to operator inattention to detail, resulted in a violation
(Section 01.5).
Isolation of the wrong air supply to residual heat removal (RHR) valves
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during out-of-service activities due to inattention to detail by the EA,
resulted in a violation (Section 01.6).
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A violation was identified lertaining to an inadequate test procedure
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which contributed to a two lour delay in recognizing an LCO entry and
taking appropriate action when the 2A atmospheric relief isolation valve
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did not satisfy stroke time testing requirements.
Some operators also
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exhibited a non-conservative approach to operability (Section 03.1).
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A violation was identified involving an inadequate test procedure which
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resulted in an inoperable penetration pressurization air compressor and
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inadvertent LCO entry. The lack of a cuestioning attitude by a
maintenance technician also contributec to this event (Section 03.2).
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Maintenance
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Informal maintenance contractor work practices resulted'in inappropriate
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cross-connecting of the service air and demineralized water systems
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(Section M1.1)
Poor material condition of two check valves resulted in two radioactive
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gas releases in the Auxiliary Building and the Unit 1 containment,
respectively.
Initial licensee investigation of the releases was
deficient (Section M2.1).
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A violation was identified involving an inadequate maintenance procedure
which resulted in a loss of instrument air (IA) to the Unit 2
containment during installation of valve blocks on the IA containment
isolation valves. An inadequate pre-job brief and deficient
communications between departments also contributed to this event
(Section M3.1).
A violation was identified involving a failure to correctly assemble two
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pressurizer power operated relief valves (PORVs) in accordance with
procedures during modifications, which resulted in the failure of one of
the PORVs.
Repairs required a plant shutdown (Section M4.1).
The inspectors identified a violation pertaining to the licensee's
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failure to ensure that a quality control (OC) inspector remained
independent of a maintenance activity involving reassembly of the 2B EDG
jacket water cooler end cover, which the OC inspector was witnessing.
The mechanic and OC inspector were also not familiar with the correct
bolting torque sequence (Section M7.1).
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Enqineerina
A violation was identified involving an inadequate leak rate testing
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procedure which did not provide sufficient configuration controls,
resulting in the inadvertent transfer of 500 gallons of water from the
Unit 2 reactor water storage tank to the refueling cavity.
The failure
of an operator to follow verbal direction also contributed to this event
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(Section E1.1).
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A violation was identified involving the inadvertent omission of a test
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procedure step by a system engineer which resulted in actuation of the
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2A servi.ce water pump breaker (Section E4.1).
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The inspectors identified a violation involving an unauthorized
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temporary alteration. A fan was taped on the Unit 2 manipulator crane
over the refueling cavity while fuel assemblies were being moved
(Section E4.2).
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Report Details
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Summary of Plant Status
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At the beginning of this inspection period. Unit 1 was at 100 percent power.
The unit was taken off-line on August 27 to repair an inoperable pressurizer
PORV. The unit was placed back on-line on September 18 and operated at
100 percent power for the remainder of the inspection period.
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Unit 2 began this inspection period at 100 percent 30wer and remained there
until September 19 when it was taken.off-line for tle start of a refueling
outage.
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Operational performance during the inspection period was characterized by
frequent operational events, several of which resulted in inadvertent LCO
entries.
The licensee was ineffective in preventing personnel errors.
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adverse trend in personnel errors was the subject of escalated enforcement.
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and corrective actions were described in the licensee's response dated
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September 27, 1996, to the Notice of Violation and Proposed Imposition of
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Civil Penalty - $50,000 (NRC Inspection Report Nos. 50-295:304/96007)).
Furthermore, several procedures were deficient, resulting in water spills and
other events.
Several of the events occurred as a result of problems in
maintaining appropriate configuration of plant systems during testing and
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other work activities.
Examples are described in the following report
sections.
Although some examples were identified by the licensee, these
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examples are included in the cited violations because their causes are similar
to previous underlying performance problems that thc licensee has not yet
effectively addressed.
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I. Operations
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Conduct of Operations
01.1
Inadvertent LC0 Entry for Isolation of Component Coolina Water (CCW)
Flow to the 2B Safety In.iection (SI) Pumo
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a.
Inspection Scone (71707)
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On September 15, the Unit 2 control room received two unexpected alarms.
" Safety injection Cooling Water Low Flow" and " Charging Pump Cooling
Water Low Flow." The ins]ectors interviewed operations department
personnel and inspected t1e involved equipment.
b.
Observations and Findings
The unexpected alarms were caused by equipment attendant (EA) actions
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while performing daily operator rounds.
The Unit 2 Auxiliary Building
EA partially disassembled the 2B SI pump CCW flow transmitter in an
effort to reset the SI pump cooling water low flow annunciator, even
though the annunciator was not alarming.
This action caused magnetic
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decoupling of the local indicator.
In an attempt to recover local flow
indication, the EA shut the CCW isolation valve to the pump which
caused one of the unexpected alarms.
Since the SI pump would not have
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performed its required safety function while CCW was isolated, the EA's
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actions caused an inadvertent entry into the LCO for TS 3.8.2.C.
During the subsequent performance of operator rounds, the EA found the
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2A charging pump cooling water flow high.
In an attempt to return the
flow to the expected range, the EA lowered flow sufficiently to cause
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another unex)ected alarm in the control room.
In both of these
instances, t1e EA did not communicate with the control room before
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performing the manipulations.
The inspectors determined th t no formal training had been provided to
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operations personnel on the manipulation of flow transmitters to clear
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an annunciator. However, during the previous week, while returning a
residual heat removal (RHR) pump to service, local indication for CCW to
the RHR pump was lost.
In response to guidance received from an
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instrument maintenance supervisor, the same EA was directed to isolate
and slowly re-establish flow. This previous evolution caused the EA to
erroneously believe his routine duties included partial disassembly and
manipulation of the flow transmitter without the need for additional
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controls.
c.
Conclusions
The inspectors concluded that:
(1) the EA did not consistently
communicate with the control room before manipulating components in the
field which had a potential to cause control room annunciators: (2) the
EA partially disassembled and manipulated a flow instrument without any
controls: and (3) based on interviews with operations department
personnel. EA duties and responsibilities were not consistently
understood within the Operations Department.
Zion Administrative Procedure (ZAP) 1200-08, " Risk Significant On-line
Maintenance," Revision 4, required:
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In Section F.1.d that the Risk Management Team identify
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compensatory measures and actions required to remove, test. or
restore the system to service for each voluntary entry into an LC0
or risk significant combination.
In Section F.3.a. that the Work Control Center pre-plan and
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coordinate work activities by all involved work departments in
order to minimize the downtime of out-of-service systems and the
risk of losing redundant equipment.
In Section F.5, that the Work Control Center be responsible for
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initiating Attachment A " Voluntary LCO Entry Outage Approval
Form."
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The failure to establish work controls, as required by ZAP 1200-8. for
the work activities associated with the 2B SI pump CCW flow transmitter
is considered a violation of 10 CFR Part 50. Appendix B. Criterion V
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(50-295/96014-01a. 50-304/96014-01a), as described in the attached
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01.2 Positive Reactivity Addition During Indications of Control Rod Position
Misalignment
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Inspection Scone (71707)
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The inspectors observed Unit 1 startup activities on Septemoer 16-17
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which were conducted in accordance with General Operating Procedure
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GOP-2, " Plant Startup," Revision 9. and Operations Special Procedure
OSP-96-016, "RCS Dilution to Criticality," Revision 0.
b.
Observations and Findings
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On September 16, the inspectors observed the infrequently performed
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evolution shift briefing for OSP-96-016.
The inspectors also observed a
subsequent control room operator briefing which was conducted just prior
to commencing the control rod withdrawal. This second briefing was held
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as a result of an eight hour delay in the initiation of the control rod
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withdrawal and to focus the shift on the evolution.
The inspectors were concerned that the guidance provided by operations
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management / supervision on how to resolve expected control rod position
indication deviation alarms, was different for each briefing.
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the infrequently performed evolution briefing, the operations manager
communicated the expectation that every deviation alarm would be
corrected prior to continuing with rod withdrawal.
However, during the
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control room shift briefing, the shift engineer, unit supervisor, and
nuclear group supervisor stated that when rod position indication
exceeded 12 steps from the demand position, the nuclear station operator
(NS0) shall stop pulling rods and evaluate the deviation to determine
whether the deviation was a rod misaligrment or a position indication
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problem.
If the deviation was due to red position indication, the NSO
shall continue withdrawing control rods to the desired position.
Once
the rods were at the desired position, the rod position indication
system would be re-aligned.
The inspectors identified, through questioning of shift personnel
immediately following the briefing, that confusion existed regarding TS
requirements for control rod alignment and position indication.
The
inspectors discussed with operators the appropriateness of withdrawing
control rods while in a TS LCO for rod position indication. An
Independent Safety Engineering Group representative noted that shift
personnel were unable to answer the inspectors * questions and he raised
a concern with operator confusion in this area to licensee management.
In response, the operations manager discussed the issue with shift
personnel and clarified the proper response to rod position deviation
alarms.
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During the withdrawal of shutdown bank D, the inspectors identified that
rod position indication appeared to deviate by greater than twelve steps
near the top of the rod pull.
The inspectors subsequently determined,
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through interviews with selected operations personnel, that on several
occasions during the withdrawal of shutdown banks, the NSO continued to
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pull control rods even though control board rod demand and rod position
indication deviated by greater than twelve steps.
The NSO indicated his reason for continuing with the rod withdrawal was
that the qualified nuclear engineer had stated that the computer was
indicating an acceptable alignment. However, the inspectors were
concerned with this justification because the computer-did not give real
time data and only provided information useful for evaluating rod
position when rod motion had stopped and the computer had time to
complete updating,
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Conclusions
The inspectors concluded that:
(1) the infrequently performed evolution
briefing was ineffective at communicating licensee management's
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expectations-for conduct of the startup: (2) command and control of the
shutdown bank control rod withdrawal was weak; and (3) due to known rod
position indication problems, the shift performing the shutdown bank rod
withdrawal was not sensitive to adding reactivity when control rod
indication was outside TS rod alignment limitations.
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TS 6.2.1.a recuired that written procedures be prepared, implemented,
and maintainec for procedures listed in Appendix A of Regulatory
Guide 1.33, Revision 2 dated February 1978. Appendix A of this
regulatory guide specified nuclear startup as an example of a general
plant operating procedure. General Operating Procedure GOP-2, " Plant
Startup," Revision 9. Step 4.0.15, required, in part, that if any
control rods were misaligned, refer to Abnormal Operating Procedure
A0P-2.1, " Rod Control System Malfunction " and contact the Qualified
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Nuclear Inspector for further guidance. Appendix C. " Stuck Rod,
Misaligned Rod, or Inoperable RPI [ rod position indication]," of A0P-2.1
required, in part, that RPI be checked against the process computer.
Failure to stop pulling control rods and enter A0P-2.1 when the control
board RPI display indicated rod misalignment, is considered a violation
of TS 6.2.1.a (50-295/96014-02).
01.3 TS Action Reouirements Not Completed Within the Reouired Time Frame
a.
Insoection Scone (71707)
The inspectors observed portions of emergency diesel generacor (EDG)
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operability surveillances and reviewed the TS required actions
associated with the 28 EDG outages of August 12-13 and September 9-11,
and the 2A EDG outage of September 15-17.
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b.
Observations and findings
The inspectors identified that on two occasions during the
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September 9-11. 2B EDG outage. the licensee exceeded the required
eight-hour time interval between ver-ifications of the availability of
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off-site power sources.
The inspectors also identified four additional
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examples during the EDG outages conducted on August 12-13 and
September 15-17, where the required 8-hour interval between verification
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of off-site power sources was exceeded.
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The inspectors determined that the failure to perform TS actions in the
required time frame was a recurring problem.
This deficiency was
attributable to a misconception that a 25 percent extension could be
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applied to the time interval of repetitive action re
manner similar to that allowed for TS surveillances.quirements in a
A similar problem
was identified with different TS action requirements, as documented in
NRC Inspection Report 50-295:304/96-16.
c.
Conclusions
The ins)ectors concluded that the failure to perform TS actions for
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inopera)le EDGs within the required time frame resulted from an
incorrect understanding of TS. Technical Specification 3.15.2.C
required demonstration of the availability of two sources of off-site
power at least once every eight hours while the 2A or 2B EDGs were
out-of-service (00S). The failure to verify the availability of two
sources of off-site power at least once every eight hours while the 2A
and 2B EDGs were 00S, is considered a violation of TS 3.15.2.C
(50-304/96014-03), as described in the attached Notice of Violation.
01.4 3.000 Gallon Demineralized Water Soill in Unit 2 Containment
a.
Inspection Scone (71707)
On September 22, 3,000 gallons of demineralized water were spilled
inside Unit 2 containment.
The inspectors interviewed operations
personnel and inspected demineralized water valve, 20W-0035.
b.
Observations and Findings
In preparation for the Unit 2 outage, licensee personnel opened two
demineralized water containment isolation valves to supply water to the
containment for use by station personnel.
The five demineralizer water
service taps downstream of the isolation valves were normally closed
between outages, and the licensee therefore assumed that these valves
were closed at the time the containment isolation valves were opened.
However 2DW-0035, located on the 560' elevation of the reactor coolant
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pump deck, was open. As a result, water sprayed from the open tap
inside the missile barrier where it collected in the containment sump.
The containment sump water level set point was reached which
automatically started the containment sump pumps.
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A radwaste operator observed indication that the sump pumps were
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running. This unexpected condition was communicated to the control room
shift engineer (SE) and the health physics (HP) supervisor, who
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subsequently dispatched an HP technician into containment to
investigate. The HP technician took immediate corrective action to shut
the valve. The licensee determined that approximately 3,000 gallons of
demineralized water had been sprayed inside the Unit 2 containment.
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At the conclusion of this inspection period, the licensee's
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investigation was still in progress.
However, the licensee tentatively
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planned to revise the station shutdown procedure to require that
operations . personnel verify that valves off the demineralized water
header were closed prior to opening the containment isolation valves.
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c.
Conclusions
The inspectors concluded that General Operating Procedure GOP-4
" Plant
Shutdown and Cooldown," Revision 13, was inadequate, in that it failed
to require verification of the position of demineralized water service
tap valves prior to opening the containment isolation supply valves.
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This is not considered a violation of NRC requirements because the
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affected valves are nonsafety related and therefore, are not subject to
Appendix B of 10 CFR Part 50.
01.5 Procedure Steos Missed While Performing EDG Surveillances
a.
Insoection Scone (71707)
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On October 6, the licensee identified that the 1A EDG was incorrectly
unloaded during shutdown when a licensed operator failed to perform a
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fifteen minute hold at one megawatt (MW). The inspectors reviewed the
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surveillance results and different revisions of procedures, and also
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interviewed the unit supervisor and several NS0s.
b.
Observations and Findings
During shutdown of the 1A EDG in accordance with surveillance procedure
PT-11-DG1A, "1A Diesel Generator Loading Test," Revision 6.
Attachment 1. the operator was required to reduce power from 4 MW to
1 MW and hold the generator power at 1 MW for 15 minutes.
However, the
operator reduced power from 4 MW to 0 MW and failed to hold power at
1 MW.
The inspectors subsequently reviewed the results of EDG surveillances
performed during this inspection period and identified that on
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September 9, the "0" EDG was run unloaded for seven minutes vice the
15 minutes recuired by surveillance procedure PT-11-DG0, "O Diesel
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Generator Loacing Test," Revision 7, Attachment 1.
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c.
Conclusions
The inspectors concluded that this event was caused by inattention to
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detail by the licensed operator.
The failures to follow surveillance
. procedures PT-11-DG1A and PT-11-DG0 for proper unloading of the EDGs
following the respective surveillance tests, are considered a violation
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of 10 CFR Part 50, Appendix B. Criterion V (50-295/96014-Olb.
50-304/96014-01b), as described in the attached Notice of Violation.
01.6 Out-of-service (00S) Errors on the Residual Heat Removal (RHR) System
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a.
Insoection Scone (71707)
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On October 7, arr equipment attendant (EA) identified two 00$' errors
while performing independent verification for two RHR system 00S tasks.
The inspectors interviewed the EA and the shift engineer. The
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inspectors also reviewed the 00S documentation and walked down the
affected portion of the RHR system.
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b.
Observations and Findings
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Two EAs were performing a " child" (subordinate) 00S task on the RHR
system. Out-of-service Nos. 960006991 and 960009514 directed the EA to
close the instrument air (IA) supply to RHR system valves 2HCV-RH606 and
2HCV-RH618, res)ectively, by closing valves 2IA0662 and 2IA0663 which
would isolate t1e main air sup)ly to each respective RHR valve.
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However, the EAs isolated the Jackup air supply to the RHR valves
instead of the main air supply.
The 00Ss were hung between 10:00 a.m.
and 1:00 p.m. on October 7.
An EA, on the following shift, was
performing an IV of the two 00$s and identified the errors. The
licensee took immediate corrective action to isolate the main air supply
and unisolate the backup air supply.
During interviews, an EA stated he did not have a complete picture of
how the plant was being configured which contributed to his course of
action.
The EA considered that isolating the backup air supply was
correct because he was performing a " child" 005 which he believed should
not isolate the main air supply. The EA further stated that the
" parent" 005, which was to be hung later, would actually isolate the
main air supply to the RHR valves.
An incorrect location on the 00S sheet also contributed to the EA's
actions. The sheet identified the 542' elevation of the Auxiliary
Building as the location for isolating the main air supply to the RHR
valves.
But, the backup air supply, rather than the main air supply,
was located on this elevation.
c.
Conclusions
The inspectors concluded that this event was primarily caused by the
EA's incomplete knowledge of the intended plant configuration.
The
independent verification process barrier was effective in identifying
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the 00S error.
However, the failure of the EAs to remove the main air
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supply to valves 2HCV-RH606 and 2HCV-RH618 from service in accordance
with the DOS procedure is considered a violation of 10 CFR 50.
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Appendix B, Criterion V (50-295/96014-01c, 50-304/96014-01c). as
described in the attached Notice of Violation.
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Operations Procedures and Documentation
03.1
Inadvertent LCO Entry for Containment Isolation Valves
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a.
Insnection Scone (71707)
On September 18, the licensee identified that a TS LC0 for containment
isolation valves had been inadvertently entered during stroke testing of
the 2A atmospheric relief isolation valve.
The inspectors reviewed the
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completed surveillance, Inservice Testing (IST) Evaluation
No. 10-9-96-3, and discussed the issue with an IST engineer.
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b.
Observations and Findings
On September 18, in preparation for the Unit 2 shutdown, the licensee
cleared the 00S for the 2A atmospheric relief isolation valve.
This isolation valve had been 00S for main control board
position indication work. The subject valve was then stroked per
PT-27G-ST, " Steam Generator PORV Stroke Time Testing," Revision 1, for
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return-to-service. The valve's stroke time of 63.2 seconds was greater
than the action value, which was an operability threshold: however, the
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valve was not declared inoperable. Acceptable results were obtained
during a second stroke test and MS-0017 was returned to service.
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Two hours after the surveillance test had been completed, a licensed
shift supervisor (LSS) who was reviewing the test results, determined
that the motor-operated valve (MOV) was technically inoperable and that
the appropriate four hour LC0 action statement for TS 3.9.3,
" Containment Isolation Valves." had not been entered.
The LSS directed
that a manual isolation valve, which had been reopened following the
test, be closed to comply with the TS.
c.
Conclusions
The inspectors concluded that PT-27G-ST was inadequate in that the
procedure did not ensure that the valve stroke time was evaluated for
acceptability by the personnel performing the test. Step 8 of
Section 5.1 of PT-27G-ST required a yes or no answer for " stroke time in
the acceptable range." However, this step did not reference
Section 5.5, " Concluding Procedure," for guidance on actions to take
when valve stroke times are outside of the acceptable range.
S]ecifically, Step 1 of Section 5.5 required that an entry be made in
tle Unit Operator's Log that the valve was inoperable based on test
results in the action range.
This step also required sign-off by a LSS,
which was not done at the time that the valve was stroked.
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-In addition. ZAP 300-02. "Use of Procedures in Operating Department."
Revision 10. Attachment 2. " Valve Stroke Timing." required that if any
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valve stroke time was greater than the action limit then the valve
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immediately be declared inoperable.
Procedure PT-27G-ST did not ensure
that the intent of ZAP 300-02 would be met. The failure of PT-27G-ST to
ensure a timely. operability evaluation of valve stroke time testing
results was considered a violation of 10 CFR Part 50. Appendix B.
Criterion V (50-295/96014-04a. 50-304/96014-04a), as described in the
attached Notice of Violation.
The failure of operators and the unit supervisor to recognize that valve
2MOV-MS-0017 should have been considered inoperable when stroke time
testing requirements were not met, regardless of the
deficiency, indicated a' lack of questioning attitude. procedure
Guidance in
Generic Letter 91-18. "Information to Licensees Regarding Two NRC
Inspection Manual Sections on Resolution of Degraded and Nonconforming
Conditions and On Operability." clearly indicates that when test
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performance data falls in the required action range. the valve must be
immediately declared inoperable. Using the results of a second stroke
time test to conclude that the subject valve was operable following-
initial test failure, without interim evaluation and/or appropriate
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corrective action, reflected a non-conservative approach to operability
determinations by the involved operators and supervisor.
03.2 Inadvertent LCO Entry for Inocerable Penetration Pressurization (PP) Air
Comoressors
a.
Inspection Scone (71707)
On October 5. the licensee identified that Unit 1 had inadvertently
entered into TS LCO 3.9.2.B.a. " Penetration Pressurization Systems."
The inspectors interviewed the unit supervisor and site quality
,
verification (SOV) personnel involved with this event.
b.
Observations and Findings
The licensee was performing Technical Staff Surveillance (TSS) 15.6.123
" Leak Test of PP Check Valves." Revision 8. for Unit 2.
The Unit 2 PP
compressor had previously been taken 00S in accordance with the
surveillance procedure. The procedure required the technician to lift
the Unit 2 lead for the PP header low pressure signal. Another lead for
automatic start of the "0" PP air compressor was at the same terminal
point. When the technician lifted both leads and re-landed the lead for
compressor automatic start, the "0" PP air compressor was rendered
However, this momentary inoperability of the "0" PP air
compressor was not recognized until pointed out by SOV personnel in the
control room.
Site Quality Verification personnel idertified that the
applicable drawing differed from the actual wiring configuration.
The
licensee subsecuently determined that, in all cases, the, approved
procedure woulc have rendered the "0" PP air compressor inoperable
resulting in an LCO entry per TS 3.9.2.B.a.
13
.'
c.
Conclusions
'.
The inspectors concluded that the technician exhibited a lack of
questioning attitude by lifting the additional lead without first
ensuring a complete understanding of the possible consequences.
In
addition. TSS 15.6.123 was inadequate.
The failure of TSS 15.6.123 to
indicate the existence of an automatic start lead that would render the
"0" PP air compressor inoperable when lifted, was considered a violation
of 10 CFR Part 50. Appendix B, Criterion V (50-295/96014-04b,
50-304/96014-04b), as described in the attached Notice of Violation.
08
Miscellaneous Operations Issues
08.1 (Closed) LER 50-304/96006-00:
Licensed shift supervisor error resulted
'
On June 12, the Unit 2 containment isolation valve, 2FCV-VN02A, was
taken DOS to repair an open limit switch.
Two licensed shift
supervisors failed to obtain the appropriate post-maintenance testing
(PMT) requirements from the system engineer.
Each licensed shift
supervisor independently and incorrectly determined that surveillance
procedure PT-300-ST, " Containment Isolation Valve Stroke Time
Verification," was sufficient to prove valve operability.
Both
individuals were confident of their knowledge regarding the appropriate
PMT requirement. After the test was completed, the valve was declared
On August 7, an NSO identified that surveillance procedure PT-40-300,
" Valve Remote Position Indication " should also have been included in
the PMT requirements for the valve. After identifying this deficiency,
the licensee took the appropriate actions to return the valve to
service.
Valve FCV-VN02A provided a containment isolation function
according to UFSAR Table 6.2-4.
Therefore, when the valve had been
returned to service on June 12, without performing the required testing,
an inadvertent entry into TS 3.9.3 occurred.
The licensee's corrective actions included:
Returning the valve to service.
-
Counseling the involved individuals, and
l
-
Discussing this event with other operators by January 1997.
-
'
The failure to accomplish the appropriate PMT activity in accordance
with the applicable procedure, PT-40-300, before declaring containment
)
isolation valve 2FCV-VN02A operable, is considered a violation of
!
10 CFR Part 50, Appendix B, Criterion V (50-304/96014-05).
Other
examples of inadvertent LCO entries due to the failure to perform
appropriate PMT are described in NRC Inspection Re) ort No. 50-295/96007:
'
50-304/96007. Hwever, these instances involved tle failure of
engineering to specify PMT when requested, whereas the inadvertent LC0
entry associated with containment isolation valve 2FCV-VN02A occurred
because the PMT requirements specified by operations personnel were
I
'
14
[
incorrect.
The inspectors concluded that the corrective actions for the
events discussed in IR 96007 would not have precluded the event
'
involving 2FCV-VN02A from occurring.
Therefore. this licensee-
.
identified and corrected violation is being treated as a Non-Cited
Violation, consistent with Section VII.B.1 of the NRC Enforcement
Policy.
Continuing inspector concern with inadvertent entries into LC0
action statements are discussed in other sections of this report.
'
II. Maintenance
M1
Conduct of Maintenance
M1.1 Contract Maintenance Worker Cross Connected Service Air (SA) and
'-
Demineralized Water Systems
a.
Insoection Scone
The inspectors reviewed the recovery action following cross-connection
of the demineralized water system with the SA system.
The problem was
identified when a worker in the Unit 2 containment noticed water flowing
from a SA valve and notified the control room.
b.
Observations and Findings
On October 8, a contract worker attempted to clear a blockage on a steam
system valve. Apparently, the worker had been successful in clearing
blockages at another plant by connecting SA and demineralized water with
a "Y" connector.
With air 2ressure higher than #r pressure, the
resultant mixture blew out tie blockage.
However, at Zion the
demineralized water system is at a higher pressure than the SA system
and as a result, the SA system was partially filled with water when the
systems were cross-connected.
Demineralized water and SA were isolated
to the containment until the "Y" connector was discovered and
disconnected and repairs and cleanup were completed.
'
The licensee directed the contractor to stand down from all work and
brief workers on proper control of maintenance.
The contractor
committed to revise pre-job checklists and walkdowns, and make additions
to its new employee orientation. The licensee commenced a root cause
investigation of the incident.
c.
Conclusions
The event appeared to be the result of informal work practices.
However, the work stoppage, work control briefings, and root cause
'
investigation were appropriate.
The root cause investigation was
hampered by the fact that the contractor fired the employee and removed
him from the site before the licensee could interview him.
15
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M2
Maintenance and Material Condition of Facilities and Equipment
~,
M2.1 Poor Material Condition of Two Check Valves Resulted in Two Gas Releases-
.
a. ..Insnection Scope (62703)
On October 5, there were two radioactive gas releases in the Auxiliary
Building and the Unit 1 containment, respectively. The inspectors
interviewed the unit supervisor, NSO, and mechanical maintenance lead:
' reviewed the plant and instrumentation diagrams (P& ids) and appropriate
procedures: and walked down the associating piping.
,
b.
Observations and Findings
.
,
The Unit 1 volume control tank (VCT) hydrogen regulator valve,1VC8155,
was repaired by maintenance personnel because it was not working
properly. After the maintenance activity was complete, an equipment
operator (EO) was sent to adjust the regulator.
The E0 performed a
bubble tesi. around the fittings and found that the fittings were
leaking. A check valve, 1VC8411, was also leaking which allowed
contaminated gases and hydrogen to escape from the VCT through the
regulator fittings into the Auxiliary Building, contaminating personnel,
During a non-related activity, the licensee was lowering VCT pressure by
venting the VCT to the waste gas system.
Check valve 0WG9280 leaked and
released contaminated gases from the VCT into the Unit 1 reactor coolant
drain tank (RCDT), which pressurized it.
The relief valve for the RCDT
opened and vented the gases to the containment sump, which caused a
containment radiation alarm. The licensee immediately stopped the
venting process and entered Abnormal Operating Procedure 5.1.
A sample
taken by the radiation protection personne1 confirmed the alarm.
The licensee's initial review of this event was deficient.
The licensee
did not identify that the source of the contaminated gases from the VCT
to the Auxiliary Building was through a failed check valve until pointed
out by the inspectors.
c.
Conclusions
The inspectors concluded that poor material condition of the check
valves caused the radioactive gas releases. The failure to initially
identify that a leaking check valve allowed gases to escape from the VCT
into the Auxiliary Building, indicated a lack of questioning attitude by
operations and maintenance personnel.
16
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M3
Maintenance Procedures and Documentation
.
'
M3.1 Loss of Instrument Air (IA) to Unit 2 Containment
,
i
a.
Insoection Scone (62703)
.
On September 25, 1996, the licensee identified that IA had been lost to
the Unit 2 containment as a result of a maintenance activity involving
the installation of valve blocks on IA containment isolation valves,
2FCV-IA01A and B.
The inspectors reviewed the results of the licensee's
investigation and the maintenance procedures used during the work
4
l
activity.
b.
Observations and Findings
Maintenance procedure M015-1, " Valve Block Fabrication. Installation,
and Removal " Revision 2, required the installation of a hand loader
'
when installing a valve block on an air operated valve.
The hand ioacer
would maintain the valve in the desired position during the valve block
installation.
However, the procedure did not contain any guidance to
,
i
ensure control of plant system configuration during the installacion of
the hand loader.
By observing the limit switches for valve 2FCV-1A01A,
the mechanics incorrectly determined that the valve was closed when in
-
fact, the valve was open.
Believing that valve 2FCV-1A01A should remain
closed, the mechanics isolated air to the valve actuator in order to
'
disconnect the air line and connect the hand loader.
This resulted in
the valve shutting which caused a loss of IA to containment.
Instrument
air was restored 32 minutes later.
'
During the pre-job briefing for this activity, the licensee specified
that the subject valves sMuld be left " blocked open." However, the
need to reposition the vahes based upon the as-found condition was not
'
discussed at this briefing.
c.
Conclusions
The inspectors concluded that:
(1) the pre-job brief was deficient
,
since it did not discuss the expected as-found position of the valves.
(2) mechanical maintenance did not contact the control room before
operating a plant system valve, and (3) Maintenance Procedure M015-1 did
4
not contain sufficient guidance to prevent the inadvertent isolation of
IA to containment.
The failure of M015-1 to provide appropriate guidance to control the
configuration of plant systems during the installation of a hand loader
was considered a violation of 10 CFR Part 50, A)pendix B, Criterion V
-
(50-295/96014-04c, 50-304/96014-04c), as descri]ed in the attached
i
17
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_
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_
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M4
Maintenance Staff Knowledge and Performance
.
1
M4.1 Mis-installation of Hynoid Kev Resulted in Failure of Power Onerated
Relief Valve (PORV) Block Valve
a.
Insnection Scone (62703)
I
On August 26, in preparation for isolating PORV block valve, RC-8000B,
in order to replace the PORV block valve stem and yoke in response to
Information Notice 92-60, " Valve Stem Failure Caused by Embrittlement,"
the valve tripped on thermal overload.
The licensee visually verified
1
that the valve was closed and attempted to manually stroke open the
,
valve, but was not successful. On August 27, Unit 1 was shut down to
repair the valve. The' inspectors discussed the event with maintenance
engineering 3ersonnel and reviewed the maintenance procedures for
assembling t'le motor-operated valve (MOV) actuator.
b.
Observations and Findings
The PORV block valve tripped on thermal overload.
The licensee
-
calculated that the thrust applied to the valve was 35,000 lbs., with
the nominal thrust window being 9,200 to 11,000 lbs. Attempts to
manually open the valve resulted in several broken gear teeth on the
valve's handwheel. Upon disassembly of the valve actuator, the licensee
identified that the locating pin associated with the hypoid gear was
.
missing.
The hypoid gear 0)erates the limit switch.
Without the
locating pin in place, the typoid gear could rotate on the drive sleeve,
rendering the limit switch inoperable.
No internal problems with the
valve were evident. The valve seat, disc, and guide were penetrant
tested with acceptable results.
The valve's failure was caused by a maintenance error.
During the
Fall 1995, Unit 1 refueling outage, maintenance personnel modified six
MOV actuators from Limitorque SMB-00 to SB-00 style actuators.
Following the PORV block valve failure, the licensee disassembled all
six valves and identified that two block valves were missing the
locating pins.
The other four valves had the locating pin correctly
installed.
In addition, the licensee identified that among 51
safety-related Unit 1 MOVs, work had been performed on 10 of the valves
during which the locating pin could have been removed. The licensee
selected five valves based on relative risk significance and inspected
each valve to determine if the locating pin was installed.
No
discrepancies were identified.
Based on the inspection results. the
licensee determined that the Unit 1 MOVs were operable.
While Unit 2 did not have any SB-00 style actuators, the licensee
identified 12 safety-related MOVs that could have missing locating pins
due to previous work performed. The licensee planned to inspect 5 of
the 12 MOVs during the Unit 2 refueling outage.
This decision was based
i
on the absence of identified problems during inspection of the Unit 1
MOVs.
18
[
c.
Conclusions
1
Maintenance Procedure P/M016-2N, "Limitorque Motor-0perated Valve
Actuator SMB-00," Revision 2, required the installation of the locating
pin and hypoid gear on the NOV drive sleeve.
However, during the 1995
Unit 1 refueling outage, maintenance Jersonnel failed to install the
hypoid gear locating pin on two PORV ] lock valve drive sleeves.
The
failure to follow procedure P/M016-2N is considered a violation of
10 CFR Part 50, Appendix B Criterion V (50-295/96014-01d,
50-304/96014-01d), as described in the attached Notice of Violation.
M7
Quality Assurance in Maintenance Activitie's
M7.1 Incorrect Torouinq Technioue During 2B Emergency Diesel Generator (EDG)
Maintenance and Inadeouate Quality Control (OC) Insnection
a.
Inspection Scone (62703)
On September 9, the 28 EDG failed the monthly operability surveillance
test due to high lube oil temperature.
The inspectors interviewed
maintenance and OC personnel, observed selected portions of the
maintenance activities associated with the inspection and cleaning of
the lube oil and jacket water coolers, and observed the replacement of
the EDG intercooler and the lobe oil temperature control valve.
b.
Observations and Findings
The inspectors observed that mechanical maintenance 3ersonnel performing
the maintenance activities were generally knowledgea]le of their
assigned task.
The mechanics placed an appropriate emphasis on foreign
material exclusion control. Work packages were available at the work
location and were used by the mechanics.
The work packages were also
adequate, based on the inspectors review.
However, the inspectors identified that an improper torque sequence was
used by the mechanic during the reassembly of the 2B EDG jacket water
cooler end cover.
The inspectors were concerned that the OC inspector
performing the inspection of the joint reassembly did not identify the
use of an improper torque sequence.
The licensee considered reassembly
of mechanical joints within the skill-of-the-craft, and as a result, a
torque se
In
addition,quence was not specified as part of the work procedure.
the OC inspector was not independent of the maintenance
activity since the inspector was setting the torque wrench for each
torque increment.
During an interview with the QC inspector, the insJectors learned that
the OC inspector's training background was not meclanical in nature, and
that he did not know the proper torque sequence for reassembly of
mechanical joints. The OC inspector was aware of the recuirement to
remain independent from the work activity being inspectec , however, he
involved himself in the work activity by setting the torque wrench.
19
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_ - - - - - -
1
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j
c.
Conclusions
-
1
,
j
The ins)ectors concluded that:
(1) the mechanic performing the
.
i
reassem)ly of the 2B EDG jacket water cooler end cover used an impro)er
torque sequence. (2) the OC inspector performing the inspection of t1e
i
torquing of the end cover was not knowledgeable of the proper torque
.
sequence for the reassembly of mechanical joints, and (3) the QC
t
inspector was not independent of the work activity since he set the
I
torque wrench for each torque increment. A similar problem was
.
identified involving an inadequate quality control inspection during EDG
j
maintenance in NRC Inspection Report 50 N /96006. 50-304/96006.
<
_
ZionIdministrativeProcedure(ZAP)520-08."StationOCInspection
'
~~
Program for Maintenance Work." Revision 3(G). requires, in part. that
j
independent inspection / quality verification be performed by qualified
4
individuals other than the group performing the maintenance task.
The
>
'
failure to ensure that the quality control inspection of the jacket
water cooler end cover reassembly was independent of the work activity.
i
in accordance with ZAP 520-08. is considered a violation of 10 CFR
'
Part 50. Appendix B. Criteria X (50-304/96014-06). as described in the
i
attached Notice of Violation.
i
.l
III. Enaineerina
El
_ Conduct of Engineering
!
b
El.1 Safety-Related Pinino Sunnort Anchor Plates Exceeded the Soecified Gao
Criteria Between the Plate and the Building Structure
a.
Inspection Scone (37551)
During plant tours and system walkdowns, the inspectors identified
piping supports with gaps between the building structure and the piping
support anchor plate.
b.
Observations and Findinos
On September 3. during a tour of the Auxiliary Building, the inspectors
identified at least ten examples of piping supports for the containment
spray and safety injection (SI) systems with gaps between the building
structure and the support anchor plate. As described in Nuclear Station
Work Procedure NSWP-S-05. " Concrete Expansion Anchors." Revision 3.
Section 6.20. the acceptance criteria for the gap between the building
structure and the piping support anchor plate is less than or equal to
1/32 of an inch, not to exceed 30 percent of the length of the anchor
plate, for each side of the plate.
In response to this issue, the licensee initiated a Problem
Identification Form and performed limited scope walkdowns of the SI and
auxiliary feedwater systems in order to better characterize the
i
magnitude of the issue.
The walkdowns revealed that 15 of the 29 piping
'
20
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, _ _ , - - - -
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_ _ .
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_ ___ - _ _ - _ _______
,
.
1
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supports inspected had gaps in excess of the acceptance criteria
!
specified in NSWP-S-05. The license initiated an o)erability assessment
,
'
to determine if the piping supports could perform t1eir intended
.
function with the gaps present.
'
c.'
Conclusions
!
The issue with piping supoort gaps exceeding acceptance criteria is
j
considered an Inspection Follow-up Item (50-295/96014-07:
50-304/96014-07) pending NRC review of the licensee's operability
l
assessment and supporting engineering calculations.
In addition, a
related issue involving the failure of VT-3 inspections, conducted-in
,
i
accordance with the inservice inspection program. _t,o include
verification of the clearance between the building structure and the
,
i
piping support anchor plate, was discussed in NRC Inspection Report
"
50-295/96013., 50-304/96013.
i
{
E1.2 Hiah Ambient Temoerature in 125 Volt-DC Battery Room
a.
Insoection Scope (37551)
,
-
.
On September 3. during a walkdown of the 011 125 Volt-0.C. station
!
battery, the inspectors identified that the ambient temperature of the
1-
battery room was abnormally high. The inspectors reviewed the results
)
of a surveillance test performed earlier in the day, the logs for
auxiliary operator tours, and battery vendor information.
b.
Observations and Findings
The inspectors noted that the licensee had perfobmed maintenance
procedure EMSP-01. " Station Battery Monthly and Quarterly Surveillance"
on September 3.
During the surveillance test, the licensee identified
that the ambient tem)erature for the 011 battery room was approximately
99 Fahrenheit (F) w1ile the expected value was between 60 and 90 F.
The licensee attributed the cause of the high ambient temperature to the
closed position of the battery exhaust fan discharge damper.
The
!
licensee determined that the damper had failed closed.. The licensee
started the redundant train of ventilation, but did not evaluato the
hydrogen concentration of the room before initiating ventilation flow.
.
As a result, the licensee was unable to use the hydrogen concentration
to determine the approximate duration that the exhaust ventilation
system had been inoperable and therefore was not able to evaluate the
'
associated operability of the battery.
,
Through a review of auxiliary operator logs, the inspectors determined
that o)erability of the battery exhaust ventilation system was checked
'
daily )y verifying that the exhaust fan was energized rather than
verifying that air flow existed.
In addition, the expected range for
the battery pilot cell temperature specified in licensee procedures was
between 60 and 100 F.
However, the nominal temperature range specified
in battery vendor information was between 60 and 90 F.
21
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._
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c.
Conclusions
.
'
Zion Operability Determination Manual guidance allows the 011 125
.
Volt-D.C. battery to be considered operable for five days without
battery room exhaust . ventilation.
This issue is considered an
-
Inspection Follow-up Item (50-295/96014-08: 50-304/96014-08) pending NRC
'
review of the basis for this guidance and operation of the battery in an
"
environment with an ambient temperature greater than that specified by
!
the vendor.
t
!
E1.3 Inadvertent Transfer of 500 Gallons of Water From the Refuelina Water
j
Storace Tank (RWST) to the Refuelina Cavity
!
a.
Insoection Scoce (37551)
l
-
!
On September 26, during testing performed by system engineering,
4
500 gallons of water were inadvertently transferred from the Unit 2 RWST
to the refueling cavity.
The inspectors interviewed operations
4
1
department personnel and reviewed both Technical Staff Surveillance
!
(TSS) 15.6.108, "S
1
j-
the control room "pecial Type B and C Leak Rate Test," Revision 3, and
posted instruction drawing."
<
j
b.
Observations and Findings
i
While performing TSS 15.6.10B for the refueling cavity to refueling
j
!
water purification pump (RWPP) valve, 2SF8767, a drain path was created
between the Unit 2 RWST and the refueling cavity.
Valve 2SF8758 (RWST
to RWPP valve) had been left open after filling the transfer canal with
i
water from the RWST to support fuel moves.
The drain path was created
I
when valve OSF0012, the refueling cavity to RWPP containment isolation
4
valve, and valve 2SF8767 were opened during the surveillance test.
The surveillance procedure for TSS 15.6.10B was inadequate in that it
did not require verification of initial valve positions to assure that a
leakage path was not created during the-performance of the surveillance
test.
In addition, a barrier that should have prevented the inadvertent
water transfer from the RWST failed. in that a non-licensed operator did
not follow the Unit 2 supervisor's direction to review the Posted
Instruction Drawing. This drawing provided the status of the valves in
the spent fuel pit cleanup and cooling systems, and had the operator
referred to this drawing, he may have recognized that specific valves
were not positioned for performance of the surveillance test.
c.
Conclusions
The failure of TSS 15.6.10B to require verification of initial valve
positions contributed to the inadvertent transfer of 500 gallons of
water from the Unit 2 RWST to the refueling cavity and is considered an
example of a violation of 10 CFR 50, Appendix B Criterion V
(50-295/96014-04d, 50-304/96014-04d), as described in the attached
Notice of Violation. The failure of a non-licensed operator to follow
verbal direction also contributed to this event.
22
i
I
?
.
E3.1 Review of UFSAR Commitments
-
~
The discovery of a licensee operating its facility in a manner contrary
.
to the Updated Final Safety Analysis Report (UFSAR) description
highlighted the need for a special focused review that compares plant
practices, procedures and/or parameters to the UFSAR descriptions.
The
i
inspectors reviewed the applicable portions of UFSAR that related to the
areas inspected. The inspectors verified that the UFSAR wording was
consistent with the observed plant practices. procedures, and/or
parameters.
'
l
E4
Engineering Staff Knowledge and Performance
E4.1 Inadvertent Plinio Breaker Actuation Due to Engineerina Personnel Error
a.
Insoection Scoce (37551)
On September 23. a system engineer did not perform the action required
in a 3rocedural step resulting in actuation of the 2A Service Water (SW)
pump 3reaker while it was racked out in the test position.
The
inspectors interviewed the system engineer and the electrical engineer
-
supervisor and reviewed the procedure and electrical prints.
b.
Observations and Findinos
'
While performing Technical Staff General Procedure (TSGP) 97. " Test of
the Autostart Inhibit Circuitry for Bus 47 Pumps." the system engineer
signed off a step which was not yet performed.
This step directed the
system engineer to energize undervoltage relay 427TD1 before
de-energizing relay SDR/27-2. When the system engineer did not perform
this step and de-energized relay SDR/27-2 the logic was satisfied for
automatic closure of the 2A SW pump breaker. The pump breaker had
previously been racked out to the remote test position. and thecefore,
closing of the pump breaker did not cause the SW pump to start,
c.
Conclusions
Inattention to detail and lack of self-checking by the system engineer
resulted in the failure to perform a required procedural step causing
closure of the 2A SW pt,1mp breaker.
The failure to ensure undervoltage
relay 427TD1 was energized prior to de-energizing relay SDR/27-1. in
accordance with TSGP 97, is considered an example of a violation of
10 CFR Part 50. Appendix B. Criterion V (50-295/96014-01e.
50-304/96014-01e) as described in the attached Notice of Violation.
E4.2 Unauthorized Temocrary Alteration of the Unit 2 Manioulator Crane
a.
Insoection Scope (37551)
On October 4. the inspectors observed that a fan was taped to the Unit 2
manipulator crane over the refueling cavity while fuel assemblies were
being moved. The inspectors interviewed involved system engineers and
23
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. _. __ _ .. _ _ . _ _ . _ _ _ _ _ . . _ _
_._________ _
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their supervisor, fuel handling personnel, and an administrative
-
,
'
operating engineer, and reviewed ZAP 510-05 " Temporary Alteration
.
Program." Revision 4.
!
.
b.
Observations and Findings .
While observing fuel moves, the inspectors noted that a fan was taped to
the manipulator crane. The fan was being used to blow air to cool the
manipulator crane motor and the pilot generator. The licensee concluded
that the fan was originally taped to the crane to address the generation
,
of heat due to excessive use of the jogging function while performing
incore shuffling of the fuel assemblies.
After the licensee decided to Jerform a full core offload for the
refueling outage, the use of t1e jogging function was limited.
However,
the fan was not removed and the crane was never tested for operation
without cooling from the fan. The condition with the taped fan had
existed since the late 1970's and the licensee had not determined
whether or not use of the fan impacted the function of the manipulator
crane.
The licensee planned to remove the fan from the crane and test the
operation of.the crane without additional cooling.
If additional
cooling was warrarited, the licensee planned to install the fan according
to ZAP 510-05 requirements and process an exempt change to install a
permanent fan.
c.
Conclusions
Zion Administrative Procedure (ZAP) 510-05, " Temporary Alteration
Program." Revision 4. defines a temporary alteration (TA) as an
j
alteration made to the plant configuration, including equipment and
facilities, intended to be temporary, that does not conform to approved
drawings or other plant documents.
The failure to process a TA for the installation of a portable fan on
'
the Unit 2 fuel manipulator crane in accordance with design controls
specified in ZAP 510-05 is considered a violation of 10 CFR Part 50,
Appendix B. Criterion III (50-304/96014-09) as described in the attached
,
V. Manaaement Meetinas
XI
Exit Meeting Summary
The inspectors ) resented the inspection results to members of licensee
management at tie conclusion of the inspection on October 21, 1996.
The
licensee acknowledged the findings presented.
'
The inspectors asked the licensee whether any materials examined during the
inspection should be considered proprietary.
No proprietary information was
. identified.
24
X2
Management Meeting Summary
-
'.
On October 7. a public management meeting with Comed was held in Region III.
The topic of discussion was the continuation of personnel errors at Zion and
the licensee's plans to stop this trend.
-
.
25
.
-
.
,
~
Partial List of Persons Contacted
-
.
..
Licensee
'
3. Mueller Site Vice President
G. Schwartz, Station Manager
W. Stone, Regulatory Assurance Supervisor
B. Fitzpatrick, Operations Manager
B. Giffin. Engineering Manager
j
K. Hansing, Site Quality verification Director
j
'
i
W. Strodl, Radiation Protection Supervisor
1
D. St. Clair, Work Control Manager
-
M. Weis, Services Director
~~
NRC
M. Dapas, Chief Reactor Projects Branch 2
M. Parker, Senior Resident Inspector, Palisades
R. Westberg, Acting Senior Resident Inspector
,
i
1
,
4
,
26
..
. .
.
.-.
-
.
--
-
List of Inspection Procedures Used
-
.
Engineering
Maintenance Observation
Plant Operations
-
Prompt Onsite Response to Events at Operating Power Reactors
List of Items Doened. Closed. and Discussed
Opened
'
'
50-295/304-96014-01a
Inadvertent LCO entry for inoperable SI pump
50-295/304-96014-01b
EDG was not cooled down for 15 minutes as
l
required by surveillance procedure
50-295/304-96014-01c
EAs performing 00S, isolated the backup air
supply to the RHR valves vice the main air
supply
50-295/304-96014-01d
Maintenance personnel failed to install the
hypoid gear locating key for two PORV block
valve drive sleeves
-
50-295/304-96014-01e
System engineer omitted step during surveillance
resulting in automatic closure of the 2A SW pump
breaker
50-295-96014-02
Failure to stop pulling control rods and enter
abnormal operating procedure following indicated
rod misalignment
50-304-96014-03
Failure to demonstrate the availability of two
sources of off-site power at least once every
eight hours while the 2A and 2B EDGs were 00S
50-295/304-96014-04a
Inadequate procedure for stroke time testing of
the 2A atmospheric relief valve
50-295/304-96014-04b
Inadequate procedure for leak testing of Unit 2
penetration pressurization system check valves
50-295/304-96014-04c
Failure to have a ste) in maintenance procedure
for installation of tle hand loader
50-295/304-96014-04d
Failure to have a step in test procedure for
verification of initial valve position
50-304-96014-05
Licensed shift supervisor error resulted in
50-304-96014-06
Failure of quality control inspector to remain
indepeadent of activity involving jacket water
cooler end cover reassembly
50-295/304-96014-07
IFI
Operability assessment and su) porting
engineering calculations for Jase plates gaps
50-295/304-96014-08
IFI
Basis for 125 volt battery operability without
battery room exhaust ventilation
50-304-96014-09
Unauthorized temporary alteration for portable
fan on fuel manipulator crane
27
I
Closed
,
.
50-304/96014-05
Licensed shift supervisor error resulted in missed
surveillance
50-304/96006-00
LER
Licensed shift supervisor error resulted in missed
surveillance
.
S
6
.
28
=
v
List of Acronyms
'.
Auxiliary Building
Abnormal Operating Procedure
.
Component Cooling Water
Equipment Attendant
'
E0
Equipment Operator
General Operating Procedure
i
Instrument Air
IFI
Inspection Followup Item
i
IP
Inspection Procedure
)
IR
Inspection Report
,1
ISEG Independent Safety Engineering Group
Inservice Inspection
Inservice Testing
'
IV
Independent Verification
LCO
Limiting Conditions For Operation
i
Licensed Shift Supervisor
Motor-Operated Valve
-
<
Non-Cited Violation
.
NRC
Nuclear Regulatory Commission
NSO
Nuclear Station Operator
Out-of-service
Operations Special Procedure
P&ID Plant and Instrumentation Drawing
Public Document Room
Problem Identification Form
Post-Maintenance Testing
,
PORV Power Operated Relief Valve
PP
Penetration Pressurization
'
OC
Quality Control
RCDT Reactor Coolant Drain Tank
RWPP Refueling Water Purification Pump
RWST Refueling Water Storage Tank
Service Air
Shift Engineer
Safety Injection
S0V
Site Quality Verification
TA
Tem)orary alteration
TS
Tec1nical Specification
TSGP Technical Staff Group Procedure
Technical Staff Surveillance
UFSAR Updated Final Safety Analysis Report
Unresolved Item
Volume control tank
Violation
ZAP
Zion Administrative Procedure
.
29
l