LER-1981-046, Forwards LER 81-046/01T-0.Detailed Event Analysis Submitted |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2771981046R00 - NRC Website |
|
text
T PHILADELPHIA ELECTRIC COMPANY 2301 M ARKET STREET P.O. BOX 8699 1881 -1981 PHILADELPHIA. PA.19101 (215)0414000 December 21, 1981
' k,,
\\\\
b x ;
y y
Mr.
R.
C.
Haynes, Director f'l i
Region I J/\\N 5 ICE?:
'~
Office of Inspection and Enforcement
- - Q u r
/
L/
US Nuclear Regulatory Commission R
L.
.i 631 Park Avenue j
King of Prussia, PA 19406 SUBJECT: LIC, ENS,EE E, VENT,_RE,PO,R,T P,R,OMPT _NO,TIFICA,TIO,N
Dear Mr. Haynes:
The following occurrence was reported to Mr.
R.
Blough, Region I, Office of Inspection and Enforcement on December 5, 1981.
Reference:
Docket No. 50-277 Report No.:
2-81-46/1T Event Date:
December 5, 1981 Report Date:
December 18, 1981 Facility:
Peach Bottom Atomic Power Station RD 1, Delta, PA 17314 T,ggh,n,1,qa,1,,,S,ggg(({ga,g{gn,,,R,e,{e,ggn,qq,,
Technical Speci ication Table 3.2.A defines the setpoint for the Main Steam Line Leak Detection High Temperature instruments at "less than 200 degrees P."
The action required if this cannot be met is to " initiate an orderly shutdown and have Main Steam Lines isolated within eight hours" (Tech Spec Table 3.2.A, note 28).
D,e,s,q[{gg{gn,,,qf,_thg,,,E,v,gn,g Unit 2 was operating at about 95% power when a Channel A Group I i
Isolation occurred and the " Main Steam Line (MSL) Tunnel High Temperature Trip" alarm annunciated.
"8201060329 811221 DR ADOCK 05000 g
/!/
Mr..R. C. Haynes Pago 2 The Main Steam Line temperature on the
'A' Channel was 195 degrees F, one
'B' Channel was about 190 degrees F, about 5 degrees F below the actual trip point.
These high temperatures were the result of a loss of the normal reactor building ventilation.
Based on previous occurrences of this. type, it is known that an immediate restoration of ventilation flow will carry hot air past the temperature switches and cause a Group I Isolation.
To prevent this significant reactor vessel pressure transient, the Main Steam Line temperature setpoints uere raised prior to restoration of normal ventilation.
After the ventilation was restored and the Main Steam Line temperatures returned to normal, the setpoints were reset to about 195 degrees F.
During the 20 minute period that the setpoints were above the normal setpoint, the indicators were constantly monitored to ensure that any unusual temperature increase would be detected.
The actions that were taken were the
- - same as those taken in January 1981 as authorized by an Emergency Technical Specification change.
The Shift Superintendent on duty knew of that occurrence and that a permanent revision to the Tech Specs had been submitted.
He believed that the Tech Specs had been revised to allow the setpoints to be increased for a short time.
Immediately following the event, he consulted the Tech Specs but could not find authority for this action.
Telephone Conversation with a staff engineer, the Assistant Station Superintendent, and a corporate licensing engineer determined that the revision was still pending.
P,r,,gb,a,b,1,g,,,gqqs gqqqn,qqs,,,gf,,gh,g,,,E,,gggg Before the instrument setpoints were increased, it was known that a main steam line break did not exist.
While the setpoints were above normal, the temperature was constantly monitored to detect any unusual temperature increase.
The setpoint change was made to prevent the significant reactor vessel pressure transient that would have resulted from a Group I Isolation.
ga,ggg,,,gf,,,,gh,g,,,E,ggn,g The Main Steam Line temperatures increased and caused an
'A' Channel Group I Isolation because normal reactor building ventilation flow was lost for a period of about two hours.
The ventilation flow was lost as a result of valving done to transfer equipment cell ventilation from the reactor building ventilation system to the standby gas treatment system.
This is routinely L
Mr.
R.
C. Hnynna Page 3 done to prevent a small radtoactive gas release from the Reactor Building Exhaust Ventilation Stack during the regeneration of a Reactor Water Cleanup Demineralizer.
The loss of normal reactor building ventilation flow was not detected until about two hours later when the
'A' Channel Group I isolation occurred.
The loss of normal ventilation occurred because of operator error during the transition to the standby gas treatment system.
That error was not discovered until after the event, during the investigation conducted by the operator on shift.
I mm,gd,i,a,(g,,C,o,ggge gi,,v,g,,Ac,g{gn s The Main Steam Line setpoints were restored to less than 195 degrees F as soon as the Reactor Building ventilation had been recovered and the Main Steam Line temperatures had been returned to normal.
These instruments were recalibrated within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and the setpoints were within Technical Specification limits.
Very truly yours, QT
/'
9 M.,J/ Cooney 1perintendent eneration Division / Nuclear cc:
Resident Inspector Director, NRC - Office of Inspection and Enforcement Mr. Norman M.
Haller, NRC - Office of Management &
Program Analysis e
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000277/LER-1981-001-04, /04T-0:on 801019,max Daily Chlorination Time Limit Exceeded by 30 Minutes.Caused by Personnel Error. Instructions Posted at Chlorination Control Panel,Procedure Clarified & Individual Reinstructed | /04T-0:on 801019,max Daily Chlorination Time Limit Exceeded by 30 Minutes.Caused by Personnel Error. Instructions Posted at Chlorination Control Panel,Procedure Clarified & Individual Reinstructed | | | 05000277/LER-1981-001, Forwards LER 81-001/04T-0 | Forwards LER 81-001/04T-0 | | | 05000278/LER-1981-001-01, /01P-0:on 810101, While Operating at 100% Power, During Surveillance Testing,Core Spray Pump D Was Found Nonoperable.Caused by de-energized Condition of Springs in 4 Kv Circuit Breaker.Breaker Replaced | /01P-0:on 810101, While Operating at 100% Power, During Surveillance Testing,Core Spray Pump D Was Found Nonoperable.Caused by de-energized Condition of Springs in 4 Kv Circuit Breaker.Breaker Replaced | | | 05000278/LER-1981-002-03, /03L-0:on 810109,HPCI Turbine Exhaust Inboard Drain Isolation Valve AO-5247 Failed to Stroke Fully.Caused by Cocked Valve Packing Follower Preventing Free Valve Stem Travel.Follower Realigned & Packing Retensioned | /03L-0:on 810109,HPCI Turbine Exhaust Inboard Drain Isolation Valve AO-5247 Failed to Stroke Fully.Caused by Cocked Valve Packing Follower Preventing Free Valve Stem Travel.Follower Realigned & Packing Retensioned | | | 05000277/LER-1981-002, Forwards LER 81-002/01T-0 | Forwards LER 81-002/01T-0 | | | 05000277/LER-1981-002-01, /01T-0:on 810105,reactor Core Isolation Cooling Pump Flow Indication Failed Rendering Automatic Flow Control Sys Inoperable.Caused by Electronic Failure of Square Root Extractor in Flow Control Circuitry.Extractor Replaced | /01T-0:on 810105,reactor Core Isolation Cooling Pump Flow Indication Failed Rendering Automatic Flow Control Sys Inoperable.Caused by Electronic Failure of Square Root Extractor in Flow Control Circuitry.Extractor Replaced | | | 05000277/LER-1981-003-03, /03L-0:on 810112,DPIS 2-14-43B,core Spray Sparger to Reactor Pressure Vessel Dp Switch Found Set Below Tech Spec Limit.Caused by Barton Model 288 Dp Switch Failure Due to Setpoint Drift.Switch Recalibrated & Returned to Svc | /03L-0:on 810112,DPIS 2-14-43B,core Spray Sparger to Reactor Pressure Vessel Dp Switch Found Set Below Tech Spec Limit.Caused by Barton Model 288 Dp Switch Failure Due to Setpoint Drift.Switch Recalibrated & Returned to Svc | | | 05000278/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | | | 05000278/LER-1981-003-01, /01T-0:on 810113,during Surveillance Test W/Unit at Full Power,Oil Leak of Approx 3-5 Gallons Per Minute Discovered on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm | /01T-0:on 810113,during Surveillance Test W/Unit at Full Power,Oil Leak of Approx 3-5 Gallons Per Minute Discovered on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm | | | 05000277/LER-1981-004, Forwards LER 81-004/01T-0 | Forwards LER 81-004/01T-0 | | | 05000277/LER-1981-004-01, /01P-0:on 810114,while Operating at 100% Power, During Routine Surveillance Test of Diesel Generator,Breaker E-32 Failed to Close on Request.Caused by Unidentified Mechanical Deficiencies.Breaker Replaced & Tested | /01P-0:on 810114,while Operating at 100% Power, During Routine Surveillance Test of Diesel Generator,Breaker E-32 Failed to Close on Request.Caused by Unidentified Mechanical Deficiencies.Breaker Replaced & Tested | | | 05000278/LER-1981-004-03, /03L-0:on 810126,reactor Pressure Switch PS-3-2-3-102C,which Trips Recirculation Pump a Found to Exceed Tech Spec Limit.Caused by Setpoint Drift of Static-O-Ring Pressure Switch.Instrument Recalibr | /03L-0:on 810126,reactor Pressure Switch PS-3-2-3-102C,which Trips Recirculation Pump a Found to Exceed Tech Spec Limit.Caused by Setpoint Drift of Static-O-Ring Pressure Switch.Instrument Recalibr | | | 05000277/LER-1981-005-03, /03L-0:on 810116,torus Vent Valve AO-2514 Failed to Close Upon Receipt of Group Three Isolation Signal & W/Use of Remote Valve Control Switch.Caused by Sticking Solenoid Valve Asco 8300 D9RF.Valve Freed & Replaced 810116 | /03L-0:on 810116,torus Vent Valve AO-2514 Failed to Close Upon Receipt of Group Three Isolation Signal & W/Use of Remote Valve Control Switch.Caused by Sticking Solenoid Valve Asco 8300 D9RF.Valve Freed & Replaced 810116 | | | 05000278/LER-1981-005-03, /03L-0:on 810127,setpoint of Temp Switch TS 5943 B (HPCI Steam Line Area High Temp Isolation) Found to Be Above Tech Spec Limit.Caused by Setpoint Drift.Instrument Recalibr to within Tech Spec Limits,Tested & Returned to Svc | /03L-0:on 810127,setpoint of Temp Switch TS 5943 B (HPCI Steam Line Area High Temp Isolation) Found to Be Above Tech Spec Limit.Caused by Setpoint Drift.Instrument Recalibr to within Tech Spec Limits,Tested & Returned to Svc | | | 05000278/LER-1981-006-03, /03L-0:on 810227,core Spray Logic Sys B Failed. Caused by Blown Fuse Due to Grounded Lug on Core Spray Pump Circuit Breaker D Latch Check Switch.Circuit Breaker Replaced & Lug on Grounded Circuit Breaker Repositioned | /03L-0:on 810227,core Spray Logic Sys B Failed. Caused by Blown Fuse Due to Grounded Lug on Core Spray Pump Circuit Breaker D Latch Check Switch.Circuit Breaker Replaced & Lug on Grounded Circuit Breaker Repositioned | | | 05000277/LER-1981-006-03, /03L-0:on 810117,main Steam Line D Radiation Monitor Failed & During Repairs Line a Monitor Cable Was Disconnected.Caused by Technician Error.Techniques Reviewed W/Technicians | /03L-0:on 810117,main Steam Line D Radiation Monitor Failed & During Repairs Line a Monitor Cable Was Disconnected.Caused by Technician Error.Techniques Reviewed W/Technicians | | | 05000278/LER-1981-007-03, /03L-0:on 810206,main Steam Line Monitor a Indicated Low Level Radiation Resulting in Trip Setpoint Above Tech Spec Limit.Caused by Instrument Zero Drift. Monitor Calibr & Returned to Svc | /03L-0:on 810206,main Steam Line Monitor a Indicated Low Level Radiation Resulting in Trip Setpoint Above Tech Spec Limit.Caused by Instrument Zero Drift. Monitor Calibr & Returned to Svc | | | 05000277/LER-1981-007-03, /03L-0:on 810103,average Power Range Monitor Flux Scram Trip Setting Was Outside Tech Spec.Caused by Engineer Failure to Make Adjustments to Setting Gains.Gains Reset & Personnel Reinstructed in Importance of Monitoring Gain | /03L-0:on 810103,average Power Range Monitor Flux Scram Trip Setting Was Outside Tech Spec.Caused by Engineer Failure to Make Adjustments to Setting Gains.Gains Reset & Personnel Reinstructed in Importance of Monitoring Gains | | | 05000278/LER-1981-008-01, /01T-0:on 810211,main Isolation Valve on Loop B Mistakenly Isolated Instead of Loop a Valve During Installation of Test Connection to 1-inch Containment Atmospheric Dilution Line.Caused by Wrong Valve Designation | /01T-0:on 810211,main Isolation Valve on Loop B Mistakenly Isolated Instead of Loop a Valve During Installation of Test Connection to 1-inch Containment Atmospheric Dilution Line.Caused by Wrong Valve Designation | | | 05000278/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | | | 05000277/LER-1981-008-03, /03L-0:on 810127,containment Isolation Valves SV-2978C & SV-2671A in Sample Lines to Oxygen Analyzer Failed to Close Fully.Caused by Sticking Plunger Assemblies. Valves Cleaned,Reassembled & Leak Tested on 810204 | /03L-0:on 810127,containment Isolation Valves SV-2978C & SV-2671A in Sample Lines to Oxygen Analyzer Failed to Close Fully.Caused by Sticking Plunger Assemblies. Valves Cleaned,Reassembled & Leak Tested on 810204 | | | 05000278/LER-1981-009-03, /03L-0:on 810216,during Surveillance Test,Oil Leak of 3-5 Gpm Found on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm in Oil Line Pressure Control Valve VC-210 | /03L-0:on 810216,during Surveillance Test,Oil Leak of 3-5 Gpm Found on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm in Oil Line Pressure Control Valve VC-210 | | | 05000277/LER-1981-009-03, /03L-0:on 810126,diesel Cardox Fire Protection Sys E-3 Failed to Initiate Automatically During Testing. Caused by Microswitch in Electromanual Pilot Control Valve Solenoid Circuitry Being Stuck Open,Preventing Initiation | /03L-0:on 810126,diesel Cardox Fire Protection Sys E-3 Failed to Initiate Automatically During Testing. Caused by Microswitch in Electromanual Pilot Control Valve Solenoid Circuitry Being Stuck Open,Preventing Initiation | | | 05000277/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000277/LER-1981-010-03, /03L-0:on 810127,drywell Radiation Monitor Found Out of Svc During Full Operation.Caused by No Sample Flow Through Sys Due to Manual Sample/Purge Valve Dislodged from Normal Sample Position.Valve Returned to Position | /03L-0:on 810127,drywell Radiation Monitor Found Out of Svc During Full Operation.Caused by No Sample Flow Through Sys Due to Manual Sample/Purge Valve Dislodged from Normal Sample Position.Valve Returned to Position | | | 05000278/LER-1981-011-03, /03L-0:on 810307,seven MSIVs Failed Individual Tech Spec Leakage Limits.Single Valves Failed on HPCI 2-inch Turbine Exhaust Line.Test Taps Failed on Reactor Core Isolation Cooling 10 & 2-inch Exhaust Lines.Cause Unknown | /03L-0:on 810307,seven MSIVs Failed Individual Tech Spec Leakage Limits.Single Valves Failed on HPCI 2-inch Turbine Exhaust Line.Test Taps Failed on Reactor Core Isolation Cooling 10 & 2-inch Exhaust Lines.Cause Unknown | | | 05000278/LER-1981-012-03, /03L-0:on 810428,snubber from a Recirculation Pump Discharge Header Found to Have Locking Velocity Under Compression Less than Acceptable Value.Cause Not Determined. Snubber to Be Recalibr | /03L-0:on 810428,snubber from a Recirculation Pump Discharge Header Found to Have Locking Velocity Under Compression Less than Acceptable Value.Cause Not Determined. Snubber to Be Recalibr | | | 05000277/LER-1981-012-03, /03L-0:on 810202,main Steam Line Monitor D Indicated Low Level Radiation Resulting in Trip Setpoint Above Tech Spec Limit.Caused by Instrument Zero Drift. Monitor Calibr & Returned to Svc | /03L-0:on 810202,main Steam Line Monitor D Indicated Low Level Radiation Resulting in Trip Setpoint Above Tech Spec Limit.Caused by Instrument Zero Drift. Monitor Calibr & Returned to Svc | | | 05000277/LER-1981-013, Forwards LER 81-013/01T-0.Provides Narrative Description of 810203 Occurrence Re Failure of Valves to Meet Seismic Qualification Requirements | Forwards LER 81-013/01T-0.Provides Narrative Description of 810203 Occurrence Re Failure of Valves to Meet Seismic Qualification Requirements | | | 05000278/LER-1981-013-01, /01T-0:on 810830,personnel Discovered Water Backed Up Out of Floor Drain Sys Flowing Under Railroad Doors. Caused by Blockage in Drain Sys.Blockage Cleared,Water Pumped Out & Processed Through Radwaste | /01T-0:on 810830,personnel Discovered Water Backed Up Out of Floor Drain Sys Flowing Under Railroad Doors. Caused by Blockage in Drain Sys.Blockage Cleared,Water Pumped Out & Processed Through Radwaste | | | 05000278/LER-1981-013, Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | | | 05000277/LER-1981-014-03, /03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 | /03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 | | | 05000278/LER-1981-014, Forwards LER 81-014/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-014/01T-0.Detailed Event Analysis Submitted | | | 05000278/LER-1981-014-01, /01T-0:on 810928,while in Cold Shutdown Condition W/Crd Sys Off to Support Plant Testing,Problems Were Encountered in Maintaining Vessel Level.Caused by Personnel Error & Incomplete Closure of Feedwater Stop Valve | /01T-0:on 810928,while in Cold Shutdown Condition W/Crd Sys Off to Support Plant Testing,Problems Were Encountered in Maintaining Vessel Level.Caused by Personnel Error & Incomplete Closure of Feedwater Stop Valve | | | 05000278/LER-1981-015-01, /01X-1:on 811023,offgas Sampling Sys Found Not Receiving Sufficient Flow.Caused by Sample Line Root Valve That Had Been Closed During Welding.Valve Opened & Added to Sys Checkoff List | /01X-1:on 811023,offgas Sampling Sys Found Not Receiving Sufficient Flow.Caused by Sample Line Root Valve That Had Been Closed During Welding.Valve Opened & Added to Sys Checkoff List | | | 05000278/LER-1981-015, Forwards LER 81-015/01T-1.Detailed Event Analysis Submitted | Forwards LER 81-015/01T-1.Detailed Event Analysis Submitted | | | 05000278/LER-1981-016-03, /03L-0:on 811027,during Surveillance Testing,Speed Control Problems W/Reactor Core Isolation Cooling Sys Were Observed.Caused by Electronic & Hydraulic Speed Controls Being Out of Tolerance.Adjustments Made to Components | /03L-0:on 811027,during Surveillance Testing,Speed Control Problems W/Reactor Core Isolation Cooling Sys Were Observed.Caused by Electronic & Hydraulic Speed Controls Being Out of Tolerance.Adjustments Made to Components | | | 05000277/LER-1981-016-03, /03L-0:on 810225,reactor Core Isolation Cooling Trip Throttle Valve Would Not Reset to Normally Open Position Using Limitorque Operator,Following Manual Trip. Caused by Worn Worm Gear in Trip Throttle Valve Operator | /03L-0:on 810225,reactor Core Isolation Cooling Trip Throttle Valve Would Not Reset to Normally Open Position Using Limitorque Operator,Following Manual Trip. Caused by Worn Worm Gear in Trip Throttle Valve Operator | | | 05000277/LER-1981-017-03, /03L-0:on 810318,all Inboard Sample Isolation valves,SV-2671A-SV2671G,closed.Caused by Short in Coil of dymo-type Solenoid Valve SV-2671A,which Blew Common Fuse in Control Circuit for All Seven Valves | /03L-0:on 810318,all Inboard Sample Isolation valves,SV-2671A-SV2671G,closed.Caused by Short in Coil of dymo-type Solenoid Valve SV-2671A,which Blew Common Fuse in Control Circuit for All Seven Valves | | | 05000278/LER-1981-017-03, /03L-0:on 811109,reactor Core Isolation Cooling High Steam Flow Isolation Switch Exceeded Tech Spec Limit. Caused by Setpoint Drift of Barton Model 288 Dpis.Instrument Recalibr | /03L-0:on 811109,reactor Core Isolation Cooling High Steam Flow Isolation Switch Exceeded Tech Spec Limit. Caused by Setpoint Drift of Barton Model 288 Dpis.Instrument Recalibr | | | 05000277/LER-1981-018-03, /03L-0:on 810306,local Leak Rate Test Determined Excessive Leakage from Manual Isolation Valve SV-2671A. Caused by Dirt Buildup on Seating Surface,Preventing Proper Valve Disc Seating.Valve Cleaned & Returned to Svc | /03L-0:on 810306,local Leak Rate Test Determined Excessive Leakage from Manual Isolation Valve SV-2671A. Caused by Dirt Buildup on Seating Surface,Preventing Proper Valve Disc Seating.Valve Cleaned & Returned to Svc | | | 05000278/LER-1981-018-03, /03L-0:on 811124,HPCI Turbine Steam Supply Valve MO-3-123-14 Failed Shut & Sys Declared Inoperable.Caused by Blown Fuse in Valve Motor Circuit.Fuse Replaced | /03L-0:on 811124,HPCI Turbine Steam Supply Valve MO-3-123-14 Failed Shut & Sys Declared Inoperable.Caused by Blown Fuse in Valve Motor Circuit.Fuse Replaced | | | 05000277/LER-1981-019, Forwards LER 81-019/01T-0.Vent Monitors Could Become Inoperable If Walls Collapsed During Seismic Event | Forwards LER 81-019/01T-0.Vent Monitors Could Become Inoperable If Walls Collapsed During Seismic Event | | | 05000277/LER-1981-019-01, /01T-0:on 810320,two Walls on Refueling Floor of Each Unit Found Unstable Under Effects of Dbe.Caused by Const or Design Error.Mods Completed to Walls.Mods Scheduled for Unit 3 Prior to Completion of Refueling Outage | /01T-0:on 810320,two Walls on Refueling Floor of Each Unit Found Unstable Under Effects of Dbe.Caused by Const or Design Error.Mods Completed to Walls.Mods Scheduled for Unit 3 Prior to Completion of Refueling Outage | | | 05000278/LER-1981-019-03, /03X-1:on 811121,drywell Wide Range Pressure Recorder PR-3508 Did Not Receive Signal & Was Declared Inoperable.Caused by Intentional Internal Ground in Printed Circuit Assembly.Floating Dc Sys Substituted | /03X-1:on 811121,drywell Wide Range Pressure Recorder PR-3508 Did Not Receive Signal & Was Declared Inoperable.Caused by Intentional Internal Ground in Printed Circuit Assembly.Floating Dc Sys Substituted | | | 05000277/LER-1981-020-03, /03L-0:on 810325,inboard Containment Radioactive Gas Sampler Isolation Valve SV-2671A Found Leaking.Caused by Plunger Assembly Sticking Due to Dirt Accumulation.Valve Cleaned | /03L-0:on 810325,inboard Containment Radioactive Gas Sampler Isolation Valve SV-2671A Found Leaking.Caused by Plunger Assembly Sticking Due to Dirt Accumulation.Valve Cleaned | | | 05000278/LER-1981-020-03, /03L-0:on 811207,reactor Coolant Isolation Cooling Torus Suction Valve MO-3-13-41 Failed to Stroke.Caused by Broken Indicating Rod Jammed within Guide Cap.Broken Rod Removed & Valve Successfully Stroked Electrically | /03L-0:on 811207,reactor Coolant Isolation Cooling Torus Suction Valve MO-3-13-41 Failed to Stroke.Caused by Broken Indicating Rod Jammed within Guide Cap.Broken Rod Removed & Valve Successfully Stroked Electrically | | | 05000277/LER-1981-021-03, /03L-0:on 810329,while at Full Power,Drywell Pressure Channel D Found Malfunctioning.Caused by Electronic Failure in Rosemount Model 1151 GP Pressure Transmitter. Circuit Boards on Transmitter Replaced | /03L-0:on 810329,while at Full Power,Drywell Pressure Channel D Found Malfunctioning.Caused by Electronic Failure in Rosemount Model 1151 GP Pressure Transmitter. Circuit Boards on Transmitter Replaced | | | 05000278/LER-1981-021-03, /03L-0:on 811211,D Core Spray Pump Failed to Start During Surveillance Test Due to Failure of Pump Breaker to Close.Cause Not Determined.Failed Breaker Replaced & Checked Daily for 2 Wks to Verify Core Spray Sys Operability | /03L-0:on 811211,D Core Spray Pump Failed to Start During Surveillance Test Due to Failure of Pump Breaker to Close.Cause Not Determined.Failed Breaker Replaced & Checked Daily for 2 Wks to Verify Core Spray Sys Operability | | | 05000277/LER-1981-022-01, /01T-0:on 810331,drywell Chilled Water Sys Found Draining Via Normal Waste & Storm Drains to Discharge Canal. Caused by Operator Error.Release Terminated.Addl Corrective Actions Forthcoming | /01T-0:on 810331,drywell Chilled Water Sys Found Draining Via Normal Waste & Storm Drains to Discharge Canal. Caused by Operator Error.Release Terminated.Addl Corrective Actions Forthcoming | |
|