05000366/LER-1981-067-03, /03L-0:on 810626,site Notified That Procedures Used for Checking Positions of Psw Valves Serving safety- Related Equipment Were Inadequate.Caused by Erroneous Determination That HNP2-3182 Confirms Valve Position

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/03L-0:on 810626,site Notified That Procedures Used for Checking Positions of Psw Valves Serving safety- Related Equipment Were Inadequate.Caused by Erroneous Determination That HNP2-3182 Confirms Valve Position
ML20009F722
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 07/21/1981
From:
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20009F713 List:
References
LER-81-067-03L, LER-81-67-3L, NUDOCS 8107310456
Download: ML20009F722 (2)


LER-1981-067, /03L-0:on 810626,site Notified That Procedures Used for Checking Positions of Psw Valves Serving safety- Related Equipment Were Inadequate.Caused by Erroneous Determination That HNP2-3182 Confirms Valve Position
Event date:
Report date:
3661981067R03 - NRC Website

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h U. S. NUCLEAR REGULATORY COMMISSION RC FORM 266

%i LICENSEE EVENT REPORT CONTROL stoCx:

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EVENT DESCRIFTtoN AND PROBABLE CONSECUENCES h ia 6 2) 10uring steady state power operation the site was notified by the NRC i

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inspector that the procedure used for checking the posi-l

,0,3!l site resident o621ltions of PSW vcives serving safety related ecuioment (HNP-2-3182, Plant I 1

i i 15ervice Water Pumo Goerability) was inadeauate in meeting the reouire-I

. ___j.an ts o' T ech Soecs section 4.7.1.2.5.

This is a non rece t iti ve event.

I l>i i IThere were no effects uoon Dublic health or safety due to this event, l

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41 42 43 44 47 CAUSE OESCRIPTION AND CORRECTIVE ACTIONS ii4olIThe cause of this event was the erroneous determination that HNP-2-3182 i 1 11 1 ladeauately confirmed the oosition of the valves s.ervino safety related j

l5,621leauioment.

HNP-2-3187, Plant Service Water System And Standbv Service i

14,63i IWater Suosystem Valves Position Veri fi ca ti on, was acoroved and oerformedl li ia l lon 7-19-81.

The unit is now in full comoliance.

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LER #:

50-366/1981-067 Licensee:

Georgia Pcwer Company Facility Name:

Edwin I. Hatch Docket #:

50-366

Narrative

Report t' o r 1.101 50-366/1991 %

,jn o-lo-s:, with the unit in steady state operation (2238 Mwt) '

the site was notified by the NRC site resident inspector that the procedure used for checking the positions of plant service water valves serving safety related equipment (HNP-2-3182, Plant Service Water Pump Operability) was inadequate in meet-

.ing the requirements of Tech Specs section 4.7.1.2.b (i.e. by verifying at least once per 31 days that each plant service water system or standby service water subsystem valve (manual,

power, or automatic) servicing safety related equipment that is not locked, sealed, or otherwise secured in position is in its correct position.)

This -.is_ a nonrepetitive event.

There were no effects upon public h_ealth or safety due to this event.

The cause of this event was the erroneous determination that HNP-2-3182 adequately confirmed the position of the valves serving safety related equipment.

A new procedure (HNP 3187, Plant Service Water System and Standby Service Water Subsystem Val'ves Position Verification) was generated as the

corrective action

It was approved on 7-18-81, performed on 31 and placed in the Tech Specs surveillance program on

- ith t h,-

r... p ii r e 41 the unit is n% in full c." p t i.i n s

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