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LER-1979-021, /01T-0 on 790207:during Test,Two Recirculation Pump Drive Flow Coastdown Transients Failed to Meet Level 1 Stds.Plant Taken to Higher Power for More Testing,Thereby Deviating from Fsar.Caused by Sys Vendor Error |
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| 3661979021R01 - NRC Website |
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2 l During the performance of HNP-2-10527. the two recirc pump drive flow coastdown I
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o ] During the performance of PNP-2-10627, turbine trip on November 23. 1978, both I
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Georgia Power Company Plant E. I. Hatch Baxley, Georgia 31513 s
Reportable Occurrence Repo?t No.
50-366/1979-021 Cause Description and Corrective Actionscriteria was failed General Electric in San Jose was contacted and informed of the problem. After investigating and discussing the problem General Electric gave their permission to go to the next test condition and continue testing, their justification being the insignificanca of the RPT at that point in the fuel cycle.
The responsible startup personnel for Georgia Power then requested that this be sent to them in writing.
It was received by Georgia Power and presented to management at which time it was decided to go on testing.
On February 8,1979, General Electric again contacted Geor-gia Power and told them that they believed it was a mistake to have increased power and continued tcsting after the level l criteria failure and that they could not further support Georgia Pcwer in operating the plant above 75%
power which was the power level at which the criteria failed.
This was dis-ment decided it best ty{ Electric and Georgia Power at which time Plan cussed between General take the plant to the test condition below the one at which the criteria was failed.
This decision was immediately put into
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action.
The next action taken whs an investigation of the instrumentation which was used in this tes) to determine the magnitude of the delay time in this in-strumentation that would cause the plot of the test data to fall outside of the criteria.
While this investigation was being performed it was found that the curve in the criteria was obtained from analysis which was done for 104.2%
power instead of the 75% power level at which the test was performed.
Gene r-al Electric then performed an analysis at the 75% power level and supplied a new graph for the criteria.
Using the correct graph in the criteria and the delay time found in the instrumentation it was found that the test data did pass the level 1 criteria.
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NARRATIVE
REPORT FOR LER 2-79-21 During the performance ofliNP-2-10627, the two recirc pump drive flow coast-down transient failed to meet a level l criteria.
The responsible person-nel discussed the level 1 criteria failure with the system vendor and per-caission Nas given to go on with the testing.
The plant was then taken to a higher power where testir.g was continued and not placed in a suitable hold condition per unit 2 FSAR Section 14.1.4.5 Paragraph 3 and HNP-2-10001, Administration of Startup Test Procedures.
The system vendor later recog-nized this action as an error and therefore a deviation from the FSAR.
The deviation was reported to the NRC site representative and after discus-sing the problem it was decided that the proper action would have been to contact the NRC and explain the justification,for increasing power before any action was taken to do so.
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| 05000366/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000366/LER-1979-001-03, /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | /03L-0 on 781229:in Cold Shutdown While Performing HNP-2-3154,reactor Water Level Instrument Switch 1 Was Found Inoperative Due to Broken Foot, & Switch 3 Actuated at 122.2 in H2O Input | | | 05000321/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000321/LER-1979-001-03, /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | /03L-0 on 790109:during Steady State Power at 2400 Mwt,Plant Personnel Inadvertently Opened Both Doors of Reactor Bldg 130-ft Airlock R106.For Reasons Unknown,Switch Which Allows Defeat of Interlock Was Operated | | | 05000321/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000321/LER-1979-002-03, /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | /03L-0 on 790111:during Normal Operation,Hpci Steam Supply valves,E41-F002 & E41-F003,automatically Isolated Due to Equipment Room High Differential Temp & Cold Outside Air Flowing Across Inlet Air Temp Elements | | | 05000366/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000366/LER-1979-002-03, /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | /03L-0 on 791231:in Cold Shutdown While Performing HNP-2-3456,overvoltage Trip Setpoint for Reactor Protection Sys Motor Generator Set B Was Found at 133.5 Volts Alternating Current.Caused by Setpoint Drift | | | 05000321/LER-1979-003-03, /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | /03L-0 on 790114:during Normal operation,hi-flow Alarm Occurred on Stack Effluent Radiation Monitor.Sample Pump Was Found Not Running.Restart Failed,As Did Spare Pump. Caused by Failure of Operating Pump Carbon Valves | | | 05000321/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003, Forwards LER 79-003/03L-0 | Forwards LER 79-003/03L-0 | | | 05000366/LER-1979-003-03, /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | /03L-0 on 790102:in Cold Shutdown While Performing HNP-2-3173 on Reactor Pressure Switch 2B21-N021C,setpoint Found Above 600 Psig for Switch No 2.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-004-03, /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | /03L-0 on 790119:during Performance of Procedure HNP-1-3302,armature Winding of HPCI Injecting Valve Motor (E41-F006) Burned When Valve Was Opening.Minor Internal Disorder Probably Led to Overheat | | | 05000366/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-004-03, /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | /03L-0 on 790104:review of HNP-2-3610-0 (RHR Pump Operability) Data Sheet Revealed Pump Delta Requirements Not Met.Caused by Personnel Error Resulting from New Procedures | | | 05000321/LER-1979-004, Forwards LER 79-004/03L-0 | Forwards LER 79-004/03L-0 | | | 05000366/LER-1979-005-03, /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | /03L-0 on 790103:under Frequency Trip Setpoint Found at 54.1HZ for Motor Generator Set A.Caused by pre-op Test on Sys.Surveillance Test HNP-2-3456 Contains Setpoint More Conservative than Tech Specs | | | 05000366/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005, Forwards LER 79-005/03L-0 | Forwards LER 79-005/03L-0 | | | 05000321/LER-1979-005-03, /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | /03L-0 on 790118:while Performing HNP-1-350-M,TDR G31-R616D Failed to Actuate at Its Setting of 15-s.Two-h Time Limit Exceeded W/Sys Down for Repair.Caused by Loose Screw on Diaphragm,Resulting in Component Failure | | | 05000366/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000366/LER-1979-006-03, /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | /03L-0 on 790102:reactor Pressure Instrument Ft&C, Relay 2B21-K34A Failed to Operate W/Actuation of 2B21-N021A. Caused by Open Coil | | | 05000321/LER-1979-006, Forwards LER 79-006/03L-0 | Forwards LER 79-006/03L-0 | | | 05000321/LER-1979-006-03, /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | /03L-0 on 790122:during Normal Startup,Reactor Operated Above 1% for Over 24-h W/O Critical Mass Peaking Factor Being Calculated.Caused by Computer Limitations for Low Power Operation | | | 05000321/LER-1979-007, Forwards LER 79-007/03L-0 | Forwards LER 79-007/03L-0 | | | 05000321/LER-1979-007-03, /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | /03L-0 on 790120:reactor Core Isolation Cooling Min Flow Valve (E51-F019) Failed to Close Automatically. Caused by Failure of Open Limit Switch,Resulting in Damage to Valve Operator & Torque Switch | | | 05000321/LER-1979-008-03, /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | /03L-0 on 790121:reactor Max Cooling Rate Exceeded Due to Injection of Condensate Feedwater Into Reactor Vessel During Slowdown.Caused by Pressure Decreasing Below Condensate Booster Pump Discharge Pressure | | | 05000366/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-008-03, /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | /03L-0 on 790110:reactor Core Isolation Cooling Steam Line Differential Pressure Low Switch Found to Actuate at 119 in H2O & High Switch at +122 in H2O.Caused by Switch Setpoint Drift | | | 05000321/LER-1979-008, Forwards LER 79-008/03L-0 | Forwards LER 79-008/03L-0 | | | 05000366/LER-1979-009-03, /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | /03L-0 on 790111:low Switch & High Switch of 2E51-NO18 Operated Contrary to Tech Specs.Caused by Switch Setpoint Drift.Corrected by Performance of HNP-2-5202 Procedure | | | 05000366/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009, Forwards LER 79-009/03L-0 | Forwards LER 79-009/03L-0 | | | 05000321/LER-1979-009-03, /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | /03L-0 on 790123:during Normal Operation,While Performing Maint on Reactor Water Cleanup Pumps,Personnel Unable to Sample Primary Coolant Every 4-h.Caused by Stopped Up Redundant Sample Line | | | 05000321/LER-1979-010-03, /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | /03L-0 on 790124:during Normal pre-conditional Ramp,Determined That a Reactor Coolant Chemistry Sample Could Not Be Obtained.Caused by Both Reactor Water Cleanup Pumps Being Inoperable & Primary Sample Line Clogged | | | 05000321/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000366/LER-1979-010-03, /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | /03L-0 on 790117:in Cold Shutdown,While Performing HNP-2-3820,switches 2B21-N301 F,H & L Did Not Actuate.Caused by Switch Diaphragm Failure | | | 05000321/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000366/LER-1979-011-03, /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | /03L-0 on 790117:during Normal Startup Test & Reactor in Cold Shutdown,Review of HNP-2-3160 (RHR Pump Operability) Revealed Required Flow Not Being Met.Caused by Procedural Error by Personnel | | | 05000321/LER-1979-011-03, /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | /03L-0 on 790124:while in Cold Shutdown,Both Doors of Reactor Bldg Were Opened,Violating Secondary Containment. Bracket Into Which Dead Bolt Projects Was Bent,Preventing Interlock from Functioning.Bracket Was Repaired | | | 05000366/LER-1979-012, Has Been Voided | Has Been Voided | | | 05000321/LER-1979-012-03, /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | /03L-0 on 790124:during Shutdown,High Pressure of 200 to 300 Psig Existed in RHR Heat Exchangers.Caused by Slow Leak Past E11-F015A Valve | | | 05000321/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000366/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000321/LER-1979-013-01, /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | /01X-1 on 790131:scram Received on Intermediate Range Monitor Hi-Hi Trip at Notch 26 of Rod 42-15.Caused by Notches Being Withdrawn Past Point Required to Achieve Criticality.Procedures Revised | | | 05000366/LER-1979-013-03, /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | /03L-0 on 790125:while in Refuel Mode,Control Rod & Control Rod Drive Removal Was Begun Before Performing one- Rod Out Refueling Interlock Operability Test.Caused by Omission of This Step in Procedure.Procedure to Be Revised | | | 05000321/LER-1979-013, Foward LER 79-013/01X-1 | Foward LER 79-013/01X-1 | | | 05000321/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | |
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