05000366/LER-1979-032-03, /03T-0 on 790508:during Review of Emergency Load Shed Logic Schemes,Possibility for Unnecessary Trip of Plant Svc Water Pump During LOCA Arose.Logic Schemes to Be Modified

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/03T-0 on 790508:during Review of Emergency Load Shed Logic Schemes,Possibility for Unnecessary Trip of Plant Svc Water Pump During LOCA Arose.Logic Schemes to Be Modified
ML19261D507
Person / Time
Site: Hatch Southern Nuclear icon.png
Issue date: 06/07/1979
From: Thomas Greene
GEORGIA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19261D506 List:
References
LER-79-032-03T, LER-79-32-3T, NUDOCS 7906190366
Download: ML19261D507 (1)


LER-1979-032, /03T-0 on 790508:during Review of Emergency Load Shed Logic Schemes,Possibility for Unnecessary Trip of Plant Svc Water Pump During LOCA Arose.Logic Schemes to Be Modified
Event date:
Report date:
3661979032R03 - NRC Website

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