ML18152A255

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Insp Repts 50-280/94-08 & 50-281/94-08 on 940306-0402. Violations Noted.Major Areas Inspected:Plant Status, Operational Safety Verification,Maint & Surveillance Insps & LER Followup
ML18152A255
Person / Time
Site: Surry  Dominion icon.png
Issue date: 04/19/1994
From: Belisle G, Branch M, Tingen S, York J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18152A256 List:
References
50-280-94-08, 50-280-94-8, 50-281-94-08, 50-281-94-8, NUDOCS 9405230037
Download: ML18152A255 (19)


See also: IR 05000280/1994008

Text

Licensee:

Docket Nos. :

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

50-280/94-08 and 50-281/94-08

Virginia Electric and Power Company

5000 Dominion Boulevard

Glen Allen, VA

23060

50-280 and 50-281

License Nos.:

DPR-32 and DPR-37

Facility Name:

Surry 1 and 2

Inspection Conducted:

March 6 through April 2, 1994

Inspectors:

J.

s.

Approved by: ~- A. B lisle, Section Chief

Divisi

of Reactor Projects

SUMMARY

Scope:

4/,t{q~

Dategned

l
112 /24-

Dae S-Ygned

4-J 1~/ 94-

Date(gned

This routine resident inspection was conducted on site in the areas of plant

status, operational safety verification, maintenance inspections, surveillance

inspections and Licensee Event Report followup.

Inspections of backshift,

holiday, and weekend activities were conducted on March 6, 8, 10, 13, 21 - 27,

30 and April 1, 1994.

Results:

Plant Operations functional area

The failure to open the Unit 1 B reactor coolant loop hot leg stop valve

within the 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> as required by technical specification 3.17.5.c was

identified as a violation (paragraph 3.c) .

9f25230037 940419

Pun

ADOCK ~5000280

G

.

  • pDR

2

The Unit 1 reactor heatup and startup after the refueling outage were executed

in a professional manner with the appropriate amount of management oversight.

Additionally, the initial approach to criticality was cautious and attention

to detail and self-checking was evident {paragraphs 3.d and 3.e).

Maintenance functional area

The overtime worked by Virginia Power and contractor personnel during the Unit

1 refueling outage was within established guidelines {paragraph 3.g).

Although a satisfactory post maintenance test was performed after maintenance

on accumulator check valves, the testing referenced as the post maintenance

testing requirements was not considered a meaningful test due to the low flow

rate achieved (paragraph 5.a).

Engineering functional area

The change (PAR 94-210) to the procedure used to test the accumulator check

valves was defective and resulted in a water hammer to the reactor coolant and

safety injection system piping.

The defective procedure was identified as a

non-cited violation (paragraph 5.b).

Plant Support functional area

--


*

---n

--* ---

-

--

-* **

-

  • -

Material was found in the containment sump after sump closure.

Foreign

material exclusion controls were ineffective and were identified as a weakness

{paragraph 3.b) .

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • W. Benthall, Supervisor, Licensing
  • R. Bilyeu, Licensing Engineer
  • M. Biron, Radiological Protection Engineer

H. Blake, Jr., Superintendent of Nuclear Site Services

  • R. Blount, Superintendent of Maintenance
  1. M. Bowling, Manager, Nuclear Licensing and Programs
  • D. Christian, Assistant Station Manager

J. Costello, Station Coordinator, Emergency Preparedness

J. Downs, Superintendent of Outage and Planning

D. Erickson, Superintendent of Radiation Protection

  • A. Fletcher, Assistant Superintendent of Engineering
  • 8. Hayes, Supervisor, Quality Assurance
  • M. Kansler, Station Manager

C. Luffman, Superintendent, Security

  • J. McCarthy, Superintendent of Operations
  1. J. O'Hanlon, Vice President, Nuclear Operations
  • A. Price, Assistant Station Manager

R. Saunders, Assistant Vice President, Nuclear Operations

  • E. Smith, Site Quality Assurance Manager

T. Sowers, Superintendent of Engineering

J. Swientoniewski, Supervisor, Station Nuclear Safety

G. Woodzell, Nuclear Training

Other licensee employees contacted included plant managers and

supervisors, operators, engineers, technicians, mechanics, security

force members, and office personnel.

NRC Personnel

  • M. Branch, Senior Resident Inspector
  • S. Tingen, Resident Inspector

J. York, Resident Inspector

  • A. Belisle, Section Chief
  • Attended Exit Interview
  1. Participated in Exit Interview via telephone conference call

Acronyms and initialisms used throughout this report are listed in the

last paragraph .

2

2.

Pl ant Status

Unit 1 completed a planned refueling outage during the reporting period.

The Unit achieved criticality on March 24 and was placed online on March

26.

The Unit was at 100% power at the end of the period.

Unit 2 began the reporting period at 98% power and was at 96% power at

the end of the period.

Power level was reduced during the period in

order to minimize level oscillations in the C SG.

The level

oscillations were attributed to partially blocked quatrefoils in the SG

upper tube support plates.

3.

Operational Safety Verification (71707)

The inspectors conducted frequent tours of the control room to verify

proper staffing, operator attentiveness and adherence to approved

procedures.

The inspectors attended plant status meetings and reviewed

operator logs on a daily basis to verify operational safety and

compliance with TSs and to maintain overall facility operational

awareness.

Instrumentation and ECCS lineups were periodically reviewed

from control room indications to assess operability.

Frequent plant

tours were conducted to observe equipment status, fire protection

programs, radiological work practices, plant security programs and

housekeeping.

Deviation reports were reviewed to assure that potential

safety concerns were properly addressed and reported.

a.

Review of Unit 1 Core Map

b.

The inspectors reviewed the video map of the fuel pool where fuel

assemblies were temporarily stored prior to being loaded into the

Unit 1 core.

The video displayed fuel assembly, burnable poison,

and flux suppression rod identification numbers.

The inspectors

also reviewed the Nuclear Material Handling Report for Surry 1,

Cycle 13 core onload. This report identified the control,

burnable poison, and flux suppression rods to be installed in the

individual fuel assemblies.

The inspectors verified that the

correct control, burnable poison; or flux suppression rods were

installed in the applicable fuel assembly.

The inspectors also reviewed the video tape that displayed the

fuel assemblies after being loaded into the core.

The video

showed the fuel assembly identification number and location for

each fuel assembly loaded into the core.

The inspectors verified

that the fuel assemblies were loaded into the core as specified by

the Nuclear Material Handling Report.

No discrepancies were

identified.

Containment Walkdown and Sump Inspection

On March 10, while inspecting the containment sump area, the

inspectors noted a plastic mop handle lying between the trash

racks and the outside of the vertical screens. There was no

~====-~~=========~------------- ~ -----

c.

3

apparent work activity in progress in this area.

Further inquires

by the inspectors revealed that this was designated as an FME area

and that the final containment sump FME inspection and

installation of the circular screens and trash rack panels had

been performed on March 2.

The mechanical maintenance procedure 1-MPT-1205-01, Unit One

Containment Sump Inspection and Test Setup, dated December 30, _

1993, provided instructions for assembly and closure of the sump

with necessary controls to maintain the required TS cleanliness

and restoration criteria. The procedure contained QC hold points

for verifying sump cleanliness which were signed off after the

maintenance activity had been performed.

Through a review of the sequence of events associated with this

issue, the inspectors determined that after maintenance and QC

closed out the sump on March 2, the HP group had unlocked the high

radiation area gates in this area. They placed a sock over a

drain to the sump in order to contain radioactive material that

was flushed into the area from cleaning the fuel transfer canal.

This sock (that had greater than 1,000 R meter reading) was

handled with the mop handle.

Discussions with HP personnel

revealed that the mop handle had been left in the sump area until

it was determined whether another flush of the fuel transfer canal

would have to be conducted. This decision had not been made at

the time the inspectors discovered the mop handle.

There was no documentation of the HP group's reentry into the FME

area. During discussions between the inspectors and the licensee

it was pointed out that 1-GOP-1.1, Unit Startup, RCS Heatup From

Ambient To 195 F, contained an operator signoff that the

containment sump was clean and free of foreign material prior to

final containment closure. Attachment 3, Containment Readiness

Verification, has a step with a sign off that states, "Sump

troughs and the DA Sump are clear of debris and floor grating is

in pl ace."

The inspectors determined that for this specific case, the

provisions of the GOP procedure would have ensured that a final

walk down would have been performed in the area where the mop

handle was left. However, not maintaining formal FME controls of

an area after it has been verified clean appeared to be a weakness

in training or program controls. This issue was discussed in

detail with licensee management at the exit meeting.

Placing Unit 1 Loop B In Service

On March 1, 1994, Unit 1 RCS loop B was filled in accordance with

l-OP-RC-002, RCS Fill, revision 3, and the loop was declared full

at 8:40 a.m.

TS 3.17.5.c required that the loop B hot and cold

leg stop valves be fully opened within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after filling a

loop from the RCS.

Therefore, the Bloop stop valves were

4

required to be open by 10:40 a.~.

The cold leg loop stbp valve

was opened within two hours; however, the Bloop hot leg loop stop

valve was not opened until 10:50 a.m.

Operators were aware that

the Bloop stop valves had to be opened within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and were

tracking the time. Operations identified that a violation of TS 3.17.5.c occurred when the Bloop hot leg stop valve was not

opened within two hours and initiated a DR.

The inspectors

reviewed this event and concluded that the following factors

contributed to exceeding the two hour limit:

The SRO did not adequately manage the time allotted in the

two hour LCO.

The initial attempt to open the loop B stop

valves was made with only ten minutes remaining in the two

hour LCO.

Obtaining satisfactory boron samples delayed opening the

loop stop valves.

Procedure l-OP-RC-002 required boron

samples be obtained prior to opening the loop stop valves.

The procedure required that the boron concentration in the

loop be equal to or greater than RCS boron concentration.

Several sets of boron samples were obtained and the

concentration of boron in the loop was consistently 10 ppm

less than RCS concentration.

Resolution of this issue

delayed opening the loop stop valves.

TSs did not require

that boron samples be obtained .

Procedure l-OP-RC-002 did not provide detailed instructions

for opening the hot leg loop stop valve.

The cold leg loop

stop valve is interlocked to the hot leg loop stop valve

such that the cold leg stop valve must be shut before the

hot leg valve will open.

The cold leg loop stop valve was

not fully shut when the procedure directed that the hot leg

loop stop valve be opened; therefore, the hot leg valve did

not open on the initial try. Electricians were called and

jumpered the interlock to open the hot leg loop stop valve.

Procedure l~OP-RC-002 was subsequently changed to delete the boron

sample requirements and also was changed to shut the cold leg loop

stop valve prior to opening the hot leg loop stop valve.

The TS purpose for unisolating a loop within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after filling

the loop from the RCS is to prevent the addition of positive

reactivity to the core by means of cold water or diluted boron

concentration.

In a safety evaluation prepared by the licensee,

the licensee concluded that a loop startup at Cold Shutdown would

not result in an inadvertent criticality regardless of the

temperature differential between the loops.

At the time of the

event, fuel was being loaded into the reactor vessel,

approximately 32 fuel assemblies were installed, and the A and C

loops were isolated and drained.

In addition, boron samples

obtained approximately 20 minutes prior to unisolating the Bloop

indicated that RCS and loop B boron concentration were within 10 ppm.

5

The failure to open the Unit 1 Bloop hot leg stop valve within

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> after filling a loop from the RCS in accordance with TS 3.17.5.c was identified as VIO 50-280/94-08-0l, Failure To Open

The Unit 1 B Loop Hot Leg Stop Valve Within 2 Hours.

d.

Unit 1 RCS Heatup

On March 22 and 23 the inspectors witnessed the Unit 1 heatup from

250 degrees F and 320 psig to 430 degrees F and 650 psig.

Procedures utilized for the heatup were l-GOP-1.2, Unit Startup,

RCS Heatup From 195 to 345, revision 5, and l-GOP-1.3, Unit

Startup, RCS Heatup From 345 to HSD, revision 7.

The inspectors

verified that the following were performed during the heatup:

The heatup rate was controlled in accordance with TS Figure

3.1-1 and was less that 40 degrees F per hour.

The containment spray, outside recirculation spray, and

inside recirculation spray systems were place in service

prior to exceeding 350 degrees F and 450 psig in accordance

with TS 3.4.

The motor driven AFW pumps were placed in automatic start

and AFW MOVs were open prior to exceeding 350 degrees F and

450 psig in accordance with TS 3.6.

When RCS temperature exceeded 350 degrees F the PORV low

pressure lift settings were disabled and the PORVs placed

into operation in accordance with TS 3.1.G.

The inspectors concluded that the heatup was accomplished

utilizing good command and control. Procedures 1-GOP-1.2 and 1.3

were adhered to and these procedures appeared to work well in that

operators understood them and accomplished the individual steps as

required.

e.

Unit 1 Startup From Refueling

On March 24, the inspectors witnessed the Unit 1 startup and

withdrawal of control rods to achieve criticality. Procedure

1-0P-RX-006, Withdrawal of The Control Banks to Critical

Conditions, revision 0, controlled activities up to criticality.

After the reactor was critical, reactor power was controlled at

10-s amps.

At that point, reactor physics testing commenced as

directed by the Reactor Engineer.

. .

6

During the approach to criticality, the inspectors performed

independent 1/M multiplication determinations to ensure that

criticality would be achieved within the procedure requirements.

The inspectors noted that the approach to criticality was cautious

and RO attention to detail and self-checking was evident.

Additionally, two independent groups were monitoring the operators

approach to criticality and independently calculating criticality

prediction measurements.

On March 25, the inspectors monitored physics testing including

the rod swap method of determining rod bank worth.

When the

C control bank worth was measured, the value was outside the minus

15% tolerance specified in the procedure.

The C control bank

worth was remeasured and again it was less than predicted by

approximately 15.7%. A DR was written and by procedure,

engineering and SNSOC were required to review the data prior to

increasing reactor power.

The inspectors attended the SNSOC

meeting in which the issue was discussed.

The SNSOC review was

thorough, and it was determined after discussions with NAF that

the most likely cause of the deviation of measured bank worth from

that predicted was the core model itself.

SNSOC also determined

that it was acceptable to increase reactor to< 30% so that the

in-core flux map could be performed.

NAF determined that the 30%

flux map would verify that no rods were unlatched and that no core

anomalies existed.

The flux map taken at 28.1% reactor power on March 26, was

analyzed by NAF and it was concluded that power distribution, hot

channel factors, control rod alignment, etc., were normal.

Within the areas inspected, one violation was identified.

4.

Maintenance Inspections (62703)

During the reporting period, the inspectors reviewed the following

maintenance activities to assure compliance with the appropriate

procedures.

-

a.

Rework on the Unit 1 Reactor Head Venting Subsystem

During this outage, the licensee replaced the inboard reactor head

vent valves, valve nos. 1-RC-SOV-100-Al and Bl, and repaired the

two outboard reactor head vent valves, valve nos. 1-RC-SOV-100-A2

and B2.

These valves are normally shut when the unit is at power

and a small amount of leakage through these valves has occurred

during past operations.

Work order nos. 00277612-02 and

00277614-02 were used by the mechanical maintenance group to

perform the work.

Mechanical corrective maintenance procedure

O-MCM-0409-01, Target Rock Model 79AB-008 Solenoid Operated Valve

Overhaul, dated January 25, 1994, was used for repairing the two

outboard valves.

The inspectors discussed repairing the two

valves with the system engineer and reviewed the maintenance

7

activity documentation.

No discrepancies were identified.

b.

Unit 1 Pressurizer PORVs

The inspectors reviewed WO nos. 00269833-01, 00267643-01,

00274963-01, and 00269799-01 that were used to repair the PORVs.

Maintenance personnel installed new diaphragms, replaced gaskets,

checked packing, replaced or lapped the valve seats, checked the

contact areas with a blue test, and checked the stroke and lift

points.

The inspectors reviewed the installation of new relief valves

1-IA-RV-114 and 115.

DCP 92-043, Pressurizer Safety Valve and

Loop Seal Modification/Surry/Unit 1, dated August 27, 1993,

covered installing the new relief valves. These valves were

installed specifically to protect the PORV air domes from

overpressure if the bottled air system pressure regulator should

fail. The inspectors also reviewed results for setting the lift

pressure for these two relief valves.

No deviations were

identified.

c.

Unit 1 Rod Control System Repairs

__________________________ :As noted in NRC Inspection Report Nos. 50-280, 281/94-02, rod

control card failures affected system reliability. During this

RFO, the licensee made a concerted effort to improve system

reliability through card replacement and refurbishment.

Rod

control improvements were performed per PM procedure

O-IPM~RD-CAB-002, Cleaning and Inspection of Rod Control Cabinets,

---dated January 21, 1994, and a WO written to cover each cabinet.

The repairs included replacing all 20 firing cards. The


inspectors noted that these cards were severely degraded and heat

damaged.

Additionally, the phase control, regulating circuit and

  • failure detector cards were inspected. The inspection of these

-rod control cards identified several loose solder connections and

-

_____ ::..,.:. __ -=-.:.. -=.C.---~~-'--::_-_--*aamaged components.

The cards were refurbished and reinstalled in

-the cabinets.

The loose solder connections were described by the I&C personnel

as being typical of defective cards produced by the vendor during

the 1980s and early 1990s.

The I&C personnel stated that as part

of the printed circuit board (card) production process, a form of

"wave soldering" was used to connect the individual components to

the printed circuit boards. The boards with the components

loosely attached were passed over a vat of molten solder and flux

solution at a controlled pace by a belt.

An agitating device in

the vat caused a wave of solder and flux solution to contact the

connections and form the bond.

Process variables such as

temperature, time, speed were difficult to control and resulted in

.cold soldered connections.

Cold soldered connections come loose

after time and movement and can result in card failure.

-*


d.

e.

8

Subsequent to the above repairs, several refurbished cards failed

upon initial energizing and during the Rod Control System PMT.

After the initial failures were repaired, the Rod Control System

performed without problems during the many rod movements

associated with physics testing. The licensee plans similar

repairs to the Unit 2 Rod Control System during the next RFO.

C CCHX Replacement

The inspectors monitored activities associated with removing and

replacing the C CCHX.

This was the last of the four CCHX to be

replaced by a heat exchanger with titanium tube material. The

original heat exchangers contained many plugged copper-nickel

tubes that failed due to the river water environment.

The CCHXs

were replaced using DCP 87-29, Component Cooling Heat Exchanger

Replacement.

The inspectors witnessed portions of the heat

exchanger rigging evolution and FME controls that were invoked for

open systems.

No problems were noted and the rigging and FME

controls were found acceptable.

Unit 1 B Reactor Coolant Pump Vibrations

The inspectors observed RCP 1-B being started from the control

room.

When the RCP was started on March 18, shaft vibrations

exceeded the alert level on the Bently-Nevada RCP vibration

monitor.

The alert limit is 15 mils and the danger limit is 20

mils.

With shaft vibration approximately 15 mils the operator

stopped the RCP.

The inspectors held discussions with maintenance personnel and

determined that during the present RFO the motor from the C pump

was installed on the B pump.

The licensee's review indicated that

there was a question as to the status of the balancing weights on

the coupling.

The existing weights were removed from the coupling

to establish a known condition for balancing. Several attempts to

balance the pump were unsuccessful and the data provided by the

keyphasor (reference) probe was questioned.

On March 22, the reference mark on the coupling which the

keyphasor probe monitors was ground deeper.

The keyphasor probe

was adjusted to provide a stronger reference signal and the B RCP

was restarted. The vibration readings obtained were analyzed by

the vendor representative and information was provided to the

craft as to where to place the balance weights. Several

additional runs of the RCP were necessary to complete the

balancing and the as-left readings were approximately 10 mils

vibration on the shaft and approximately 1.0 mil on the frame.

The vendor concurred that the readings obtained were acceptable.

The inspectors considered the licensee's control of vendor

activities acceptable.

However, the lack of detailed knowledge of

the vibration monitoring equipment by licensee personnel delayed

f.

9

balancing the RCP and contributed to a higher than usual number of

starts and stops of the RCP.

Coating Flaking Examination on Unit 1 HVAC

In 1977 the licensee made a design change (DC 77-32) which was

used to add ventilation ductwork to the containments. This

modification was made for both units. During later outages,

coating inspections on Unit 1 revealed areas of blistering and

delamination. These modified HVAC areas in Unit 2 only had a few

areas of blistering and delamination.

The inspectors reviewed EWR 88-517 which evaluated the potential

for transporting peeling paint from containment ductwork into the

containment sump and blocking the sump screens during a LOCA.

The

dynamic analysis showed that the floor water velocity was not

enough to transport the paint chips to the sump screens.

As part

of this engineering analysis, the coating was visually examined

and it was revealed that only the epoxy topcoat was flaking and

that the zinc primer coat remained intact. The analysis indicated

that an improper cure time of the primer coating would cause this

type of failure. It was recommended that engineering personnel

inspect the ducts during outages and have the blistered paint

_removed.

_ _ ______ _

The inspectors accompanied the licensee during the walkdown of

Unit 1 containment HVAC ductwork to ensure that no excessive

amount of loose or flaking epoxy topcoat was present. The

inspectors, in conjunction with licensee personnel, performed a

visual inspection of most of the coating on the ducts. The amount

of areas that had flaked paint varied from duct to duct. Only an

occasional, small nonadhering edge was noted.

The licensee

performed an inspection of these ducts shortly after the unit was

shutdown and any loose pieces were removed.

The inspector

concluded that the licensee had performed an adequate job in

removing the loose particles.

g.

Overtime Usage During Refueling Outages

TS 6.8.10 requires that procedures be established to insure that

the NRC policy statement guidelines regarding working hours

established for employees are followed.

This TS also requires

_documentation of authorized deviations from-those guidelines and

that the documentation be available for NRC review. Station

administrative procedure VPAP-0103, Working Hours And Limitations,

revision 3, implements TS 6.8.10. For station personnel

performing safety-related activities, VPAP-0103 step 6.5 requires

overtime hours (excluding shift turnover time) in excess of 16

hours, 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> in any 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period, 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in any 48 hour5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />

period, and 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in any 7 day period be approved by the

Station Manager and documented on Attachment 1, Request To Exceed

Overtime Hours.

Non-station personnel must adhere to their

10

department's overtime policies and obtain verbal approval from

their department superintendent, director or manager before

working more than 50 hours5.787037e-4 days <br />0.0139 hours <br />8.267196e-5 weeks <br />1.9025e-5 months <br /> per week.

These procedural

requirements were consistent with the NRC guidelines contained in

GL 82-16, NUREG-0737 Technical Specifications, and GL 82-12,

Nuclear Power Plant Staff Working Hours.

By letter dated

March 1, 1983, the NRC informed the licensee that TS 6.B.10

complied with the requirements of GL 82-16.

The inspectors reviewed records and available information to

determine if excessive overtime was routinely being utilized at

the site. For VEPCO employees, the licensee provided the

following information for the period January 1 through March 12,

1994:

Work

Percent

Max. Actual

Avg. Actual

Group

Overtime

Hrs/wk/person

Hrs/wk/person

Mechanical

29.5

31

25

Maintenance

El ectri ca 1

27.0

28

24

Maintenance


**- ---*----- *-***-*- -----

-


- ----- ----

-

Radiation

22.7

18

17

Protection

Operations

19.7

17

18

JSI/NDE

8.5

14

9

Engineering

2.2

4

I

-

To focus on overtime utilization during the present Unit I

refueling outage, three weeks of work hour information for

_

approximately 660 licensee employees were reviewed by the


----:-----=--*inspectors.

The weeks reviewed were, January 23 - 29,

--February 13 - 19, and February 20 - 26, 1994, designated week I,

week 2, and week 3 respectively.

In general, most employees

directly involved in outage activities, were working between 60

and 65 hours7.523148e-4 days <br />0.0181 hours <br />1.074735e-4 weeks <br />2.47325e-5 months <br /> a week on a six day/IO hours per day or

five day/12 hours per day work schedule.

For weeks I, 2, and 3,

the number of personnel working 65 to 69 hours7.986111e-4 days <br />0.0192 hours <br />1.140873e-4 weeks <br />2.62545e-5 months <br /> were 29, 28, and

26, respectively; 70 to 74 hours8.564815e-4 days <br />0.0206 hours <br />1.223545e-4 weeks <br />2.8157e-5 months <br /> were 30, 32, and 32,

respectively; 75 to 79 were 13, 9, and 19, respectively; and 80 to

84 were O, 0, and 4, respectively. That is, approximately 10 to

12% of the licensee's workforce worked 65 or more hours per week.

From this data and from completed VPAP-0103 Attachment I forms, 49

employees who had worked at some time in excess of the guidelines

were selected for additional analyses for the period January 23

through March 5, 1994. This period covered the beginning of the

Unit 1 outage until the end of the pay period immediately

11

preceding this inspection.

The personnel selected represented

various functions, i.e., operations, mechanical maintenance,

electrical maintenance, instrumentation and control, nuclear

material control, health physics, and engineering.

The sample

included both salaried and non-salaried personnel.

In this sample

there were 25 examples, approximately 50%, in which VPAP-0103

Attachment 1 forms had been approved in anticipation of exceeding

the guidelines; however, work records indicated the guidelines

were not exceeded.

The inspectors identified only three examples

in which personnel were authorized to exceed the guidelines in two

or more consecutive seven-day periods. Since no QA personnel were

involved in the sample, the inspectors discussed overtime

utilization by QA personnel with the Manager QA - Surry.

He

indicated that, as of March 17, 1994, he had authorized no

personnel to exceed the guidelines contained in VPAP-0103. *

Based upon these inspection activities, involving the review of

over 2,000 individual records, the inspectors determined that

licensee personnel were not routinely working excessive overtime.

Contractor overtime utilization during the outage was also

reviewed.

Work hour information involving approximately 525

contract personnel for two consecutive weeks, February 13 - 19 and

February _20 -._26, 1994_, .designated week 4 and week 5 respectively,

were reviewed.

For weeks 4 and 5, the number of personnel working

65 to 69 hours7.986111e-4 days <br />0.0192 hours <br />1.140873e-4 weeks <br />2.62545e-5 months <br /> were 21 and 15, respectively; 70 to 74 hours8.564815e-4 days <br />0.0206 hours <br />1.223545e-4 weeks <br />2.8157e-5 months <br /> were

25 and 24, respectively; and 75 to 79 hours9.143519e-4 days <br />0.0219 hours <br />1.306217e-4 weeks <br />3.00595e-5 months <br /> were 2 and 4,

respectively.

No individual worked more than 78 hours9.027778e-4 days <br />0.0217 hours <br />1.289683e-4 weeks <br />2.9679e-5 months <br /> per week in

this two week sample. That is, approximately 8 to 10 % of the

contractor workforce worked 65 or more hours per week.

From the

group that worked more than 65 hours7.523148e-4 days <br />0.0181 hours <br />1.074735e-4 weeks <br />2.47325e-5 months <br /> in one week, information for

34 contractors were examined in additional detail to determine the

daily work hour distribution. The sample included electricians,

ironworkers, welders, mechanics, valve technicians, sheetmetal

workers, insulators, painters, and lead personnel associated with

these groups.

Personnel in this sample worked between 120 and 150

hours in the two we*ek period with 13 contractors working 10 or*

more days consecutively. Records for 15 of the 34 contractors for

the subsequent week were randomly chosen to be reviewed.

The

three weeks of data for these 15 contractors revealed 2 additional

people who had worked greater than 10 days in a row.

Two

individuals, a crane mechanic and a crane supervisor, that were

previously identified as working more than 10 consecutive days

were determined to have worked at least 18 and 19 days in a row

without a day off. This was discussed with plant management.

The inspectors determined that contractor personnel were not

routinely working excessive overtime and that the overtime worked

was within established guidelines.

A review of 100 Attachment 1 forms revealed that 10 of the forms

had approval signatures dated two weeks or later than the end of

12

the time period that involved the overtime. Since verbal

approvals were sometimes obtained during nights and weekends with

the Attachments 1 subsequently completed, the inspectors were

unable to determine whether these examples represented a failure

to approve the overtime prior to its performance or reflected only

a documentation problem.

These examples were provided to the

licensee for additional review as warranted. A computer printout

was routinely provided to management to identify station personnel

that exceed the administrative limits provided in VPAP-0103.

Administrative services personnel reviewed this printout and

verified that Attachment 1 forms have been received by

Administrative Services.

When discrepancies were identified,

actions were taken to obtain the required documentation.

Within the last two years, QA performed audit no. 92-11 that

addressed Operations' overtime compliance with VPAP-0103.

The

audit report concluded that Operations personnel had received

prior approval from the Station Manager before exceeding the

limits in VPAP-0103.

One example, considered an isolated case,

was identified in which the overtime form was approved by the

Station Manager after the overtime was worked.

The audit report

also stated that substantial progress had been made by the

Operations Department in obtaining approval prior to working

overtime.

Within the areas inspected, no violations or deviations were identified.

5.

Surveillance Inspections (61726, 42700)

During the reporting period, the inspectors reviewed surveillance

activities to assure compliance with the appropriate procedure and TS

requirements.

a.

Partial Stroke Testing of Accumulator Check Valves

On March 22 the inspectors witnessed the performance of 1-PT-18.3,

Refueling Testing of Accumulators Check -valves and MOVs,

revision 1.

The purpose of this procedure was to partially stroke

the accumulator check valves and verify local and remote positions

and ERFCS indications for the accumulator MOVs.

The inspectors

witnessed the test from the control room.

The accumulators were pressurized to 650 psig and RCS pressure was

reduced until level in each accumulator decreased the required

amount.

Each accumulator discharge MOV was shut after level in

the respective accumulator decreased the required amount.

Level

in the B accumulator only dropped four percent and DR S-94-0740

was written. The inspectors reviewed the DR response which stated

that a four percent drop was acceptable.

Procedure 1-PT-18.3 was

revised to accept a four percent level decrease for one time only.

The inspectors noted that after level initially started to


13

decrease it took approximately thirty to forty minutes for level

to decrease four to five percent in each accumulator.

The

inspectors were informed that one percent of level in each

accumulator corresponds to an approximate volume of 24 gallons.

The accumulator check valves are 12 inches in diameter.

The

inspectors calculated that the flow rate through each check valve

was approximately three to four GPM during the test. The

inspectors concluded that a three to four GPM flow rate through a

12 inch check valve was not a meaningful partial stroke test due

to the low flow rate.

The accumulator check valves were full stroked tested utilizing

non-intrusive acoustic test equipment at the beginning of the RFD.

The Band C accumulator check valves were subsequently

disassembled and reassembled during the RFD.

The check valves'

discs were manually stroked during this maintenance.

If no

practical means exists to partial stroke test the valves, then

this manually stroking was an acceptable PMT.

GL 89-04, Guidance

on Developing Acceptable Inservice Testing Programs, states that,

if possible, check valves should be partial stroked following

reassembly.

At the end of the inspection period the licensee was

reevaluating this test. Options to enhance test performance and

the practicality of performing accumulator check valve partial

stroke testing were being reviewed.

b.

Close Test of Accumulator Discharge Check Valves

Procedure l-OPT-SI-010, Close Testing of Accumulator Discharge

Check Valves, revision 1, provides instructions to test the

backflow seat tightness of the two check valves in the flow path

between each accumulator and RCS cold leg. This test, was

performed on March 23 and the backflow leakage through two check

valves, l-Sl-130 and l-SI-147, Band C accumulators, respectively,

was measured at greater than 5 gpm.

The test was performed at 950

psig RCS pressure.

Based on the above tests results, the licensee decided to retest

the failed valves at a higher pressure.

Procedure l~OPT-SI-010

was changed by PAR 94-210 to test accumulator Band C check valves

at normal operating pressure.

At 2250 psig, the valves were

retested by closing the discharge MDV and measuring leakage

between the two series check valves through a test line. This

test depressurized and partially drained the piping between the

two check valves. Seat leakage test indicated that the check

valve closest to the RCS loop was seated with O flow indicated.

After completing the C accumulator check valve test, the

C accumulator isolation valve, l-SI-MOV-1865C, was reopened

according to procedure and the following was observed:

The C SI accumulator level dropped approximately 25%.

' ...

14

The 1-C RCP oil reservoir hi-lo level annunciator (B-F-7) came in and locked in.

All 3 channels of C loop low flows came in and cleared.

The 1-C RCP frame alert and danger annunciators came in and

cleared when reset.

Vibration/thud was felt in TSC and reported to the operator.

DR S-94-0755 was written to document the occurrence and the

licensee's engineering walkdown of the piping and supports did not

identify any damage.

The inspectors reviewed the operator logs and procedure, which had

been changed to retest the check valves.

The inspectors noted

that PAR 94-210, that had been approved by SNSOC prior to use,

deleted a caution from the test. The deleted caution read, "The

accumulators MOVs must be slowly jogged open in order to prevent a

possible hydraulic shock with consequent damage to system piping."

Also the procedure step to open 1-SI-MOV-1865C was changed from

"Slowly open 1-SI-MOV-1865C by jogging the control switch", to

"Open 1-SI-MOV-1865C and de-energize the valve motor operator".

In reviewing .the event., . the 1 i censee determined that a very ..

similar event had occurred on Unit 2 during the same test and the

procedure caution was to prevent recurrence.

TS 6.4.A.2 and section 17.2.5 of the QA Program Topical Report

VEP-1-5A Amendment 5 (updated 6/92) requires that technically

adequate procedures be developed and implemented as required by

Regulatory Guide 1.33, QA Program Requirements.

Regulatory Guide

1.33 invokes ANSI NlS.7-1976, Administrative Controls and Quality

Assurance for the operational phase of nuclear power plants.

Section 5.3.2(5) of ANSI NlS.7-1976 requires that procedures

contain precautions to alert individuals performing the task to

those important measures which should be used to protect equipment

and personnel.

The SNSOC approved procedure change initiated by

PAR 94-210, deleted necessary precautions which resulted in an

inadequate procedure being used and could have resulted in

equipment damage.

This was identified as NCV 50-280/94-08-02,

Inadequate Procedure Associated with Accumulator Check Valve

Testing.

The licensee initiated a root cause analysis to

identified actions to preclude recurrence. This violation will

not be subject to enforcement action because the licensee's

efforts in identifying and correcting the violation meets the

criteria specified in Section VII.B of the Enforcement Policy.

Within the areas inspected, one NCV was identified.


---------------=~----------------

__ ,_______._.:.-~-------------------------------

.

    • 6.

15

Licensee Event Report Followup (92700)

The inspectors reviewed the LERs listed below and evaluated the adequacy

of the corrective action.

The inspectors' review also included followup

of the licensee's corrective action implementation.

a.

(Closed) LER 50-280/93-002, Unit 1 Reactor Trip During Reactor

Protection System Surveillance Testing.

On February 9, 1993, a

Unit 1 reactor trip occurred due to the failure of the

A reactor trip breaker shunt trip relay during a surveillance

test. The reactor trip and the subsequent corrective actions to

restart the unit were discussed in NRC Inspection Report Nos.

50-280, 281/93-05.

In order to prevent recurrence,

a failure

analysis for the failed relay was performed and an engineering

evaluation was performed to identify single point relay failures

that could result in reactor trips. The inspectors reviewed the

failure analysis, RCE 93-03, for the failed relay. The failure

analysis was performed by the relay vendor.

The vendor concluded

that one of the relay coils was not properly insulated during the

manufacturing process which resulted in a short in the coil and a

premature relay failure.

The inspectors reviewed the Level 1 for

engineering to evaluate the reactor protection, safeguards, and

CLS logic to identify where single mode relay failures would

result in a reactor trip. The Level 1 engineering study

identified eight relays in each unit that would result in a

reactor trip if the relay failed.

The Level 1 recommended that

these relays be replaced every third RFO.

The station manager

directed that these relays be replaced ever other RFO and that the

relays be inspected during the alternate RFO.

The inspectors

reviewed the PM program and verified that the relays were

scheduled to be replaced or inspected every RFO.

Many of the Unit

1 relays were replaced during the current RFO.

b.

(Closed) LER 50-280, 281/93-006, SW Flow Path to Main Control Room

Chillers Inoperable Due to Pipe Leak.

This issue involved a

failure of strainer 1-VS-S-lA due to a leak in the strainers

backwash line. The-failed strainer resulted in an inoperable SW

flow path which resulted in entry into a six-hour LCO to HSD in

accordance with TS 3.0.1. The strainer was bypassed and the

six-hour LCO was exited.

As corrective action the strainer and

backwash line were replaced. This maintenance was inspected and

discussed in paragraph 4.a of NRC Inspection Report Nos. 50-280,

281/93-13.

c.

(Closed) LER 50-281/92-10, Relay Failure Results in Unplanned

Automatic Start of Turbine-Driven AFW Pump.

This issue involved

the unplanned start of the Unit 2 turbine drive AFW pump due to

the failure of a relay in the B train of the AFW auto start

circuit. The relay was replaced and satisfactorily tested on the

following day.

As corrective action the licensee performed CDE

131670 in order to determine why the relay failed. The CDE,

reviewed by the inspectors, concluded that the relay was original

..

16

installation and failed due to ageing.

The relay in the A train

turbine driven AFW pump auto start circuit was replaced and the

corresponding train A and B relays in Unit 1 were replaced.

Within the areas inspected, no violations or deviations were identified.

7.

Exit Interview

The inspection scope and findings were summarized on April 6, 1994, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection results addressed

in the Summary section and those listed below.

I:ll!g Item Number

VIO

50-280/94-08-01

NCV

50-280/94-08-02

LER

50-280/93-002

LER

50-280, 281/93-006 LER

50-281/92-10

Status

Open

Closed

Closed

Closed

Closed

Description/{Paraqraph No.)

Failure to Open the Unit 1 B

Loop Hot Leg Stop Valve Within

2 Hours (paragraph 3.b).

Inadequate Procedure

Associated with Accumulator

Check Valve Testing

(paragraph 5.b)

Unit 1 Reactor Trip During

Reactor Protection System

Surveillance Testing

(paragraph 6.a).

SW Flow Path to Main Control

Room Chillers Inoperable Due

to Pipe Leak (paragraph 6.b).

Relay Failure Results in

Unplanned Automatic Start of

Turbine-Driven AFW Pump

(paragraph -6.c).

Proprietary information is not contained in this report. Dissenting

comments were not received from the licensee.

8.

Index of Acronyms and Initialisms

AFW

AUXILIARY FEEDWATER -

ANSI

AMERICAN NATIONAL STANDARDS INSTITUTE

CCHX

COMPONENT COOLING HEAT EXCHANGER

CDE

CAUSE DETERMINATION EVALUATION

CLS

CONSEQUENT LIMITING SAFEGUARDS

DA

DRAINS AERATED

DCP

DESIGN CHANGE PACKAGE

DR

DEFICIENCY REPORT

ECCS

EMERGENCY CORE COOLING SYSTEM

ERFCS

EWR

F

FME

GL

GOP

GPM

HP

HSD

HVAC

l&C

IR

ISI/NDE

LCO

LER

LOCA

MOV

NAF

NCV

NRC

PM

PMT

PORV

PPM

PSIG

QA

QC

R

RCE

RCP

RCS

RFO

RO

SG

SI

SNSOC

SRO

SW

TS

TSC

VEPCO

VIO

WO 17

EMERGENCY RESPONSE FACILITY COMPUTER SYSTEM

ENGINEERING WORK REQUEST

FAHRENHEIT

FOREIGN MATERIAL EXCLUSION

GENERIC LETTER

GENERAL OPERATING PROCEDURE

GALLONS PER MINUTE

HEALTH PHYSICS

HOT SHUTDOWN

HEATING VENTILATION AND AIR CONDITIONING

INSTRUMENTATION AND CONTROL

INSPECTION REPORT

INSERVICE INSPECTION/NON DESTRUCTIVE EXAMINATION

LIMITING CONDITION FOR OPERATION

LICENSEE EVENT REPORT

LOSS OF COOLANT ACCIDENT

MOTOR OPERATED VALVE

NUCLEAR ANALYSIS AND FUELS

NON-CITED VIOLATION

NUCLEAR REGULATORY COMMISSION

PREVENTIVE MAINTENANCE

POST MAINTENANCE TESTING

POWER OPERATED RELIEF VALVE

PARTS PER MILLION

POUNDS PER SQUARE INCH GAGE

QUALITY ASSURANCE

QUALITY CONTROL

RADIATION EQUIVALENT MAN

ROOT CAUSE EVALUATION

REACTOR COOLANT PUMP

REACTOR COOLANT SYSTEM

REFUELING OUTAGE

REACTOR OPERATOR

STEAM GENERATOR

SAFETY INJECTION

STATION NUCLEAR SAFETY OPERATING COMMITTEE

SENIOR REACTOR OPERATOR

SERVICE WATER

TECHNICAL SPECIFICATION

TECHNICAL SUPPORT CENTER

VIRGINIA ELECTRIC AND POWER COMPANY

VIOLATION

WORK ORDER