ML18033B712
| ML18033B712 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 05/10/1991 |
| From: | Kellogg P, Patterson C NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18033B710 | List: |
| References | |
| 50-259-91-10, 50-260-91-10, 50-296-91-10, NUDOCS 9105210235 | |
| Download: ML18033B712 (69) | |
See also: IR 05000259/1991010
Text
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UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W.
ATLANTA,GEORGIA 30323
Report Nos.:
50-259/91-10,
50-260/91-10,
and 50-296/91-10
Licensee:
Valley Authority
6N 38A Lookout Place
1101 Market Street
Chattanooga,
TN
37402-2801
Docket Nos.:
50-259,
50-260,
and 50-296
License Nos.:
and
Facility Name:
Browns Ferry Units 1, 2,
and
3
Inspection at Browns Ferry Site near Decatur,
Inspection
Conducted:
March
16 - April 19,
1991
Inspector:
C.
spector
5
Dat
Si
ne
Accompanied
by:
E. Christnot, Resident
Inspector
W. Bearden,
Resident Inspector
K. Ivey, Resident
Inspector
G. Humphrey, Resident
Inspector
J. Brady, Reactor Inspector
N.
conomos,
Reactor Inspector
Approved by:
Ins
r grams,
TYA Projec
s Division
Date S'gne
SUMMARY
Scope:
This routine resident
inspection
included maintenance
observation,
operational
safety verification, post modification testing,
r estart test
program,
safety
parameter
display
system,
system
pre-operability
checklists,
emergency
operating
procedures,
nuclear
instrumentation reliability, Three Mile Island
action items,
information notices,
reportable
occurrences,
action
on previous
inspection
findings, condition
adverse
to quality reports,
allegations,
and
information meetings with local officials.
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POR
6
Results:
The integrated
leak rate test
was successfully
performed
on March 18,
1991.
The ten year primary hydrostatic test
was performed
on April 9,
1991.
Seven
leaking control rod drive housings
remain to be repaired.
Significant problems
were identified with the nuclear
instrumentation
affecting the
source
range
monitoring,
intermediate
range
monitoring,
and local
power range monitoring
systems.
Resolution
of these
problems
continues
with vendor
technical
assistance,
paragraph
9.
A violation with two examples
was identified for failure to implement test
control measures
for returning components
to service,
paragraphs
4 and
11.
The
first example
was for not conducting
adequate
testing for the reactor building
to
torus
vacuum
breakers.
The
breakers
opened
unexpectedly
during
the
integrated
leak rate test.
The second
example
was for not caution tagging
a
residual
heat
removal
service
water
pump awaiting post modification testing.
The
pump
was
assigned
to start for diesel
generator
testing
but failed to
start
on two occasions.
A violation
was
identified for failure to perform required
compensatory
sampling,
paragraph
3.
This was apparently
due to falsification of surveill-
ance
records.
The licensee
reported this in licensee
event report 259/91-03
on April 1,
1991.
A non-cited
violation
was
identified for inadequate
procedure
guidance
concerning
a safety assessment
for post maintenance
testing,
paragraph
15.
The
licensee initiated
a procedure
change
to correct this administrative
problem.
An unresolved
item was identified concerning technical
specification require-
ments
during instrument flow check valve testing,
paragraph
3.
Performing the
test
requires
the
core
spray
and residual
heat
removal
systems
to
be
made
because
water
level initiation instruments
are
valved
out of
service.
Five Three Nile Island Action Items,
6 Licensee
Event Reports,
6 Inspector
Followup
Items,
5
Unresolved
Items,
and
3 Violations
were
closed.
All
remaining
issues
with the Safety
Parameter
Display
System,
Restart
Human
Engineering Discrepancies,
and
Emergency Operating Instructions
were resolved.
REPORT DETAILS
Persons
Contacted
Licensee
Employees:
- 0. Zeringue,
Vice President,
BFN Operations
- L. Nyers, Plant Manager
N. Herrell, Operations
Manager
- J. Rupert, Project Engineer
- N. Bajestani,
Technical
Support Manager
R. Jones,
Operations
Superintendent
A. Sorrell, Maintenance
Manager
G. Turner, Site guality Assurance
Manager
- P. Carier, Site Licensing Manager
- P. Salas,
Compliance Supervisor
- J. Corey, Site Radiological Control Manager
R. Tuttle, Site Security Manager
Other
licensee
employees
or contractors
contacted
included
licensed
reactor
operators,
auxiliary operators,
craftsmen,
technicians,
public
safety officers, quality assurance',
design,
and engineering
personnel.
NRC Personnel:
- C. Patterson,
Senior Resident
Inspector
- E. Christnot, Resident
Inspector
- W. Bearden,
Resident
Inspector
- K. Ivey, Resident
Inspector
- G. Humphrey,
Resident
Inspector
"Attended exit interview
and initialisms
used
throughout this report are listed in the
last paragraph.
Maintenance
Observation
(62703)
Plant
maintenance
activities
were
observed
and
reviewed for selected
safety-related
systems
and
components
to
ascertain
that
they
were
conducted
in accordance
with requirements.
The following items
were
considered
during
these
reviews:
LCOs maintained,
use of approved
procedures,
functional testing and/or calibrations
were performed prior to
returning
components
or
systems
to service,
gC
records
maintained,
activities accomplished
by qualified personnel,
use of properly certified
parts
and
materials,
proper
use
of
clearance
procedures,
and
implementation of radiological controls
as required.
0
Work documentation
(MR,
WR,
and
WO) were reviewed to determine
the status
of outstanding
jobs
and
to
assure
that priority was
assigned
to
safety-related
equipment maintenance
which might affect plant safety.
The
inspector
monitored,
reviewed,
and
observed
the licensee's
maintenance
activities in the following areas:
a.
SRMs,
IRMs, and
The licensee
established
a plan, with GE, to correct
and
improve
maintenance
activities involving the nuclear instrumentation.
This
resulted
in the
generation
of numerous
and significant work
activities.
Among the items generated
were:
A method for cleaning
and installing
transmission
cable
connectors,
a
new
method for
determining
the status
of the transmission
cables,
and additional
trouble shooting methods.
b.
The licensee
completed
a
SBGT system
outage
which consisted
of SIs,
PMs,
and cleaning.
The inspector
observed
a specific
PM performed
on
temperature
switches in SBGT Train C.
c.
0
The
licensee
performed
a
major realignment
to the
following replacement
of four wiped bearings.
The high pressure
turbine
and
low pressure
turbines
were
decoupled
and
each
turbine
aligned to the next turbine.
Based
on the reviews,
observations,
and followup, the inspector
concluded
that
the
licensee
conducted
these activities
according
to procedures,
clearances
were adequate,
and personnel
involved were qualified.
No violations or deviations
were identified in'he Maintenance
Observation
area.
3.
Operational
Safety Verification (71707)
The
NRC inspectors
followed the overall plant status
and
any significant
safety matters
related
to plant operations.
Daily discussions
were held
with plant management
and various
members of the plant operating staff.
The inspectors
made
routine visits to the control
rooms.
Inspection
observations
included
instrument
readings,
setpoints
and
recordings,
status
of operating
systems,
status
and alignments of emergency
standby
systems,
verification of onsite
and offsite
power supplies,
emergency
power sources
available for automatic operation,
the purpose of temporary
tags
on
equipment
controls
and
switches,
alarm
status,
adherence
to
procedures,
adherence
to
LCOs,
nuclear
instruments
operability,
temporary alterations
in effect, daily journals
and logs,
stack monitor recorder traces,
and control
room manning.
This inspection
activity also
included
numerous
informal discussions
with operators
and
supervisors.
General
plant tours
were conducted.
Portions of the turbine buildings,
each reactor building, and general
plant areas
were visited.
Observations
included
valve
position
and
system
alignment,
and
hanger
conditions,
containment
isolation
alignments,
instrument
readings,
housekeeping,
power
supply
and
breaker
alignments,
radiation
and
contaminated
area controls,
tag controls
on equipment,
work activities in
progress,
and radiological protection controls.
Informal discussions
were
held with selected
plant personnel
in their functional
areas
during these
tours.
a.
Instrument Line Flow Check Valve Testing
The inspector
reviewed
LRED 91-2-040 which outlined
a situation where
testing
required
by
TS contradicts
with another
section of TS for
equipment operability.
To perform instrument line flow check valve
testing at greater
than
500 psi
the valve alignment
takes
out the
water level instruments for initiation of
and
RHR systems
making
them inoperable.
The initiation logic is I of 2 taken twice.
One trip system contains
A and
C instruments
and
the other trip system
contains
B and
D.
However,
instrument
leg
A contains
A and
B
and instrument
leg
B
contains
C and
D.
To perform the test,
an instrument leg is valved
out of service
which
removes
an
instrument
channel
in
each trip
system.
TS Table 3.2.B, Instrumentation
That Initiates or Controls
the
Core
and
Containment
Cooling Water,
requires
a minimum of two
instruments
per trip system.
The test
makes
Note I.B for
Table
3.2.B
applicable
and
the
system
or
component
must
be
This action contradicts
other
TS requirements
to have
(3.5.A)
and
RHR Systems
(3.5.B) operable with fuel in the vessel
at
greater
than atmospheric
pressures.
The licensee's
position is that
since the required action (to be in cold shutdown) for the inoperable
CS and
RHR has
been met, the test
can
be performed under existing TS.
The inspector
did not agree with this practice.
The
TS should
be
clarified or testing
performed without fuel in the vessel.
The
NRC
did not preapprove this test
as mentioned in the
LRED.
This item is
identified as
URI 259,260,296/91-10-01,
TS Requirements
During Check
Valve Testing.
b.
Standby
Gas Treatment
Room Flooding
During
a routine tour of the plant
on March 28,
1991, the inspector
observed
water
running across
an entrance
roadway to the
radwaste
building.
The inspector
followed the water to the
SBGT building
entrance
and
observed
water
running
out
underneath
the
entrance
door.
The inspector
entered
the
SBGT building
and notified the
control
room of the problem.
Operations
and health physics
personnel
responded
to the
scene.
The area
was
found to be not contaminated.
The source of the water
was
determined
to
be water overflowing from
a
sump.
The
has
a
keep fill system to maintain water in the
sump to minimize potential airborne contamination
problems.
The keep
fill valve
had stuck open.
The operator
banged
on
a controller that
caused
the fill valve to shut
and the
pump to start.
The
SBGT building is toured
by plant personnel
once
on each eight
hour shift.
The inspector
obtained
a printout of the
room access
from security
and
determined
that the
room
had
been
entered
four
hours earlier.
Therefore,
the water spillage
had apparently occurred
during the previous four hours.
The licensee initiated
an incident
investigation for the controller fai lure.
The inspector
concluded
that the plant tours were being conducted
and that the plant response
to this was proper.
Failure to Implement
TS Required
Compensatory
Measures
On March 1,
1991,
TVA determined
that
gaseous
and liquid effluent
compensatory
measures
were not performed
as required
by TS 3.2.D and
3.2.K for inoperable
monitors.
and Table 3.2.D,
which includes
RCW monitor
2-RM-90-132, require that grab samples
be
collected
and analyzed at least
once per 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />
when the
RCW monitor
is inoperable
and effluent releases
are
in progress.
and
Table
3.2.K,
which
includes
monitors
1-RM-90-250,
2-RM-90-250,
3-RM-90-250,
and O-RM-90-252, require that
a flow rate
estimate
be
taken
at least
once
per
four
hours
whenever
the
instruments
are declared
and effluent releases
are being
conducted
through
an affected
pathway.
On October
31,
1990, all four CAMs on the refuel floor (1-RN-90-250,
2-RM-90-250,
3-RM-90-250,
and
0-RM-90-252)
were declared
and
removed
from service for replacement.
Compensatory
monitoring
was established
per O-SI-4.8.B.l.a.2,
Airborne Effluent Release
Rate
By Manual
Sampling
When
A Gaseous
Effluent Monitor Is Inoperable.
Compensatory
monitor ing
continued
until
the
modifications
were
completed
and the
CANs declared
on January
18,
1991.
On
December
30,
1990,
the
Chemistry
section
became
aware
of
discrepancies
between
compensatory
SI data entries
and refuel floor
security access
logs.
Specifically, the sample flow data required
by
TS to be obtained
every four hours
was signed off as being obtained
by
a
RLA who, according to the security refuel floor entry log, was
not on the refuel floor where the
CANs are physically located at the
time
the flow was
recorded.
Chemistry
conducted
a preliminary
investigation
which indicated
possible
falsification
and
gA was
requested
to
perform
a
more
in-depth
investigation.
The
gA
investigation
identified
18
discrepancies
between
Chemistry
compensatory
SI data
sheets
and security logs within a
7 day period.
Of the
18 discrepancies,
17
involved
gaseous
sample
flow rate
measurements
and/or samples,
and one involved
a liquid sample.
On January
30,
1991,
gA issued
a
CARR listing the
18 discrepancies.
The licensee
found supporting
evidence
to corroborate
performance of
16 of the discrepancies.
The remaining
two discrepancies
were the
gaseous
effluent flow rate
measurement
required
by TS 3.2.K for the
four
monitors
in
the
reactor/turbine
building
and
radwaste
ventilation systems
on December
5, 1990, at 4:00 a.m.,
and the liquid
sample for the
RCW system monitor required
by TS 3.2.D
on December
11,
1990, at 10:03 a.m.
Although the
RLA had
documented
that work
activities
were
completed,
security
keycard
data
could not support
that the
RLA was in the sampling areas
at the time of sampling.
The
licensee
concluded that the
RLA did not conduct the two required
activities and, therefore,
the requirements
of TS Sections 3.2.D and
3.2.K were not met.
The licensee
reported this information to the
NRC via the
on March
1,
1991,
and
submitted
on
April 1,
1991.
The licensee
conducted
an incident investigation (II-B-91-045) which
concluded that the root cause of this event
was poor work practices.
Specifically,
RLAs signed off steps
in SIs that were not personally
performed.
A contributing factor
was attributed
to
inadequate
supervision
by the
CSS for not ensuring that compensatory
SIs were
completed
when performed.
The licensee
immediately
removed
the
responsible
for the
reportable
occurrences
from safety
related
activities.
This is considered
a violation of TS 3.2.K,
and identified as
259,260,296/91-10-02,
Missed Compensatory
Samples.
This
VIO is not a
NCV because
of the falsification of records.
Unplanned
On April 12,
1991,
at
12:34
a.m.
the outboard
MSIVs closed
due to
actuation of the
Group
1
PCIS logic.
The automatic closure occurred
while
instrument
technicians
were
valving
out
the
high
side
connection of level transmitter
2-LT-3-56B.
This occurred at step
7.6 of 2-SI-4.7.D. l.d.1, Instrument Line Flow Check Valve Operability
Test.
Although step
7.6 was expected
to initiate the
B1 logic of the
Group
I
PCIS logic by removing the
AC electrical
power supply from
the
AC solenoids for the outboard
MSIVs an isolation was not expected
since
the
DC solenoids
should
have held the
MSIVs open.
An initial
investigation
by operations
has
determined
that the
DC power supply
was interrupted to relay
16AK52 associated
with
WO 91-29308-00.
The
licensee
is still
investigating
this
event
and
an
incident
investigation
report
and
LER will be issued
when that investigation
is complete.
The inspector will review the licensee's
investigation
report when it is issued.
e.
Licensed Operator Overtime
A NRC violation was
issued at the Sequoyah facility due to
a problem
with unapproved
excessive
overtime for operations
personnel.
The
licensee
recently
revised
TVA Standard
2.1.7,
Administration of
Overtime,
as
the
result
of that
violation
to clarify the
requirements.
The inspector
determined
that
Browns Ferry currently
has
41
(31 unrestricted)
and
37
(12 unrestricted)
which
should
be more than
adequate
to satisfy all operational
requirements
without the use of routine excessive
overtime.
An inspector
reviewed
the licensee's
program at
Browns
Ferry for
ensuring
that licensed
operators
do not work overtime in excess
of
NRC guidelines identified in Generic Letters 82-02, 82-12,
and 83-14.
These guidelines
are
implemented
by TVA in SDSP 19.3, Administration
of Overtime,
and
TVA Standard
2. 1.7.
These restrictions
apply to all
employees
performing safety related
work.
Deviations
from these
restrictions
are allowed if prior approval
by the proper
management
level is obtained.
The inspector
reviewed selected
portions of the
control
room logs
and the weekly operations shift schedule for March
1 - April 15,
1991,
to determine if any apparent
discrepancies
existed for operator
overtime.
The inspector did not identify any
examples of excessive
overtime during that period.
Additionally the inspector held discussions
with Site
gA Organization
personnel
to determine
the extent of that
groups
involvement for
oversite of activities in this area.
The inspector
was informed that
the onsite
gA organization
had responded
to the Sequoyah violation by
performing
a special
monitoring report during the last part of 1990.
The inspector
reviewed portions of this licensee
monitoring report
and
determined
that
one
example of an operator
exceeding
overtime
limits had
been identified.
This discrepancy
is also identified in
CA(R
BFg900397P
and
deals
with exceeding
the
72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> in
7
days
limitation without proper authorization.
gA personnel
had reviewed
time sheets
for 75 operations
personnel
as part of this review.
The
inspector
determined that this discrepancy
was
an isolated
case.
Based
on the above reviews the inspector
determined that the licensee
has
an
adequate
program
to control
the
use of overtime
and
a
sufficient number of licensed
operators
exists
to allow restart of
Unit 2 without the use of excessive
overtime.
One violation was identified in the Operational
Safety Verification area.
4.
Post Modification Testing
(37700,
72701)
The
inspector
continued
to
observe
and
review
the
licensee's
activities.
In
a
previous
inspection,
the
inspector
noted that
the
licensee
not document
any TD's if a
PMT was
being performed
as
a testing
work plan.
The inspector
informed the licensee
that this
was considered
a significant weakness.
After additional
reviews the following was noted.
a ~
b.
c ~
d.
The inspector
noted that during the
ILRT the reactor building to
torus
vacuum breakers
opened
on positive pressure.
This indicated
that the logic for vacuum breaker
opening
was reversed.
The breakers
opened
when the pressure
on the torus
was approximate
1 psig greater
than the pressure
in Secondary
Containment.
No excessive
amount of
air was
blown into the reactor building because
the
check
valves
held.
Testing following design
change
P3051
was
inadequate.
This
item is considered
the first example of
a 'violation of 10 CFR 50
Appendix B, Criterion XI, Test Control,
and is identified as
VIO 2,'59,
260, 296/91-10-03,
Inadequate
Test Control.
The inspector
noted that during the performance of testing work plan
WP2274-90
on June
12,
1990, for System
73,
HPCI, valve 2-FCV-73-30
was inadequately
tested.
The testing work planned required that the
valve be tested
from the local control handswitch station but did not
specify
how the valve
was to be tested.
The item was signed off as
being satisfactorily tested.
Additional work activities involving
91-24404-00
on January
12,
1991,
discovered
that valve 2-FCV-73-30
would not function from the local control switch station
due to a
follow on installation.
The. valve was tested
from the control
room.
The operator
held the switch continuously
because
when
he released
the switch the valve would stop in the open position.
The switch is
a "seal-in" switch which can
be released
once actuated.
The follow
on installation
was part of
a cable
replacement.
This
item was
discussed
with the
licensee
and
a
PMT scheduled
in February
1991
should
have corrected this problem.
In
a
previous
inspection
report,
the
inspector
expressed
a
concern
involving the
licensee's
modification to the
decay
heat
removal
mode of operation for the
SBGT system.
This concern dealt
with a single failure of the
SBGT Train
B with the other two trains
operating.
During this reporting period,
the licensee
performed
a
special test with the
SBGT Train
B stopped,
the inlet damper
open
and
both trains
A and
C running.
The recorded flow up through the stack
was
16,519
cfm and
back flow though train
B was
254 cfm.
The 16,519
cfm flow up the stack
was greater
than the
16,200
cfm discussed
in
the
FSAR Section 5.3.3.7,
Standby
Gas Treatment
System.
The inspector
requested
and
received
from the licensee
a list of
testing
work plans
which were
performed
on the following systems:
System
23,
Service
Water;
System
31,
Control
Bay
HVAC;
System 57-2,
120/208 Volt AC Distribution; System 57-5,
4160 Volt AC
Distribution;
System
64,
System
67,
Emergency
Equipment
Cooling Water;
and
System
74,
Residual
Heat Removal.
The
items reviewed consisted of 31 testing
WPs which were
used to test
26
ECN/DCNs.
The system
reviews were
as follows:
System
23,
RHR Service
Water.
Testing
WP 0403-90
was written to
verify vibration readings
for
pump
A after the completion of
ECN/DCN H4330.
Testing
WP 2554-90
was originally written to perform
electrical testing of equipment associated
with System
23 affected
by
the
implementation
of
ECN/DCN
11605.
A review of the
completed
testing
WP indicated that all
PMT for System
23
had
been deleted.
The inspector
was unable to determine
why this
PMT had
been deleted.
System
31, Control
Bay
HVAC.
Testing
WP 2554-90
bump tested
the
1B
control
bay chilled
water
pump
motor for proper
rotation
in
accordance
with procedure
ECI-O-OOO-MOT00-1, for
ECN/DCN
11605;
Testing
WP 2332-90
bump tested
the
ACUs
2A and
2B drive motors for
proper rotation for ECN/DCN 10421;
and Testing
WP 2637-90 tested
the
emergency air conditioner motor for electrical
board
rooms
1A and
1B
for ECN/DCN 2242.
System
67,
Emergency
Equipment
Cooling Water.
Testing
WP2356-90
tested
the strainer
motors for A and
D and also stroke tested
valves
2-67-13
and
67-49 for
ECN/DCN
5547;
and Testing
WP 3042-90
was
written to
perform
dynamic
testing
on
pressure
control
valve
3-PCY-67-78
per
procedure
EMI-60,
Inspection
and
Preventive
Maintenance of Control
Bay Ch'illers.
In
testing
WP
3042-90,
a
reference
was
made
to
procedure
PMTP-BF-67-024.
The test
form did not indicate that
PMTP-BF-67.024
had
been
performed
or when it had
been
performed.
The inspector
noted that
some of the testing
WPs involved more than just rolling a
few wires
as initially indicated
by the licensee.
The inspector
concluded
from the
observations,
reviews,
and
followup that the
documentation
of testing
WPs activities
was
tenuous
at best.
The
inspector
was
informed that
the licensee's
gA organization
was
reviewing testing
WPs
and
had
made similar observations.
The
gA
personnel
stated
that
a
PRO
was
being
issued
to formally identify
their observations.
The licensee's
gA/Engineering Department
issued
monitoring report
gBF-R-91-1177,
Work Plan
Review for
WP Testing
Requirements,
dated April 4-5,
1991.
This report documented similar
observations
made
by the inspector.
This report also
contained
a
copy of
BFP
91
0118P which documented
the specific findings of
the
review.
The results
included
seven
improvements
to
program
items:
Instructions for handling
documentation
such
as
Form SDSP-417s
and work plans
should clear ly delineate
the final destination of
the
record
copy
and
where
the official
gA record
can
be
obtained.
Preliminary
( Information Only)
Form
SDSP-417s
in closed
work
plans
in the vault
can
cause
confusion.
Some consideration
should
be
given to either issuing/revising
Form
SDSP-417s
or
ensuring final 417s catch
up with the work plan prior to putting
in record storage.
Also,
417 forms other than official design
change notice copy should
be marked "for Information Only."
More attention to detail is needed
and
perhaps
some additional
training.
Clarification in program documents
(SDSP 17.2) that TD's are not
required for true installation tests.
Plant instructions
need to provide
space for component
unique
identification at beginning of instruction.
Instructions
need to address
under what conditions
an installat-
ion test
can
be performed,
during
PMT.
SDSP
17.2
needs
to provide instructions
to specify specific
applicable
portions of the test procedure
to be run instead of
all of the test procedure.
Based
on
the
reviews,
observations
and
followup the
inspector
concluded
that the licensee
has
resolved
the issue of testing
work
plans.
One violation was identified in the Post Modification Testing area.
5.
Restart Test Program
(71711)
During
the
reporting
per iod,
the
inspectors
reviewed
the
licensee's
restart activities
to test
and verify that
equipment will perform in
accordance
with required
sp6cifications.
In addition,
procedures
were
reviewed
and
walked-down for adequacy
determinations.
Results
of the
areas
reviewed are
as follows:
1.
Major Equipment Star t-Up and Testing
Reviewed
a 0
Reactor
Core Isolation Cooling (RCIC), System
71.
The system restart test
was performed per 2-TI-188, Reactor
Core
Isolation
Cooling,
which
included
the
performance
of
SI-4.5.F.l.e,
RCIC System
Rated
Flow At 150 PSIG, to verify the
operability of the
RCIC system
in conformance with requirements
specified
in
TS 4.5.F.l.e.
The scope
was to verify that the
RCIC turbine,
pump,
and auxiliaries could
be operated
from the
control
room and deliver
a rated flow of 600
gpm at
a discharge
pressure
of 80 psig
above
the operating
steam
pressure.
In
addition,
RTP-071,
required that the flow rate
and pressure
be
obtained within 30 seconds
from a cold start.
The inspectors
walked
down the TI prior to the test
and reviewed
this testing in progress
on March 22,
1991.
The
pump was unable
to deliver the flow at
a discharge
pressure
of 480 psig within
10
b.
the required
30 second
time period.
The discharge
pressure
was
adjusted
to slightly above
the required
330 psig
and the test
was successfully
re-performed
on March 28,
1991.
High Pressure
Coolant Injection (HPCI), System
73
An overspeed
turbine trip was
performed
on March 29,
1991 per
MMI-23.
This activity had
been attempted
on March 28,
1991, but
a malfunction in the mechanical
trip device
did not perform
correctly
and
had to
be replaced.
After the replacement,
the
unit was restarted
and the trip device
was adjusted
to trip the
unit between
4920
rpms
and
5080
rpms.
The trip occurred at
approximately
5010 rpms which met the acceptance
criteria.
The inspector
viewed the test in progress.
No deficiencies
were
noted during the
performance
of the test or with the results
obtained.
co
Reactor Recirculation
Pumps,
System
68.
The
A recirculation
pump
and
associated
equipment,
including
the
MG set,
was
run on. March 26,
1991,
as part of the plant
restart effort in accordance
with 2-0I-68, Reactor Recirculation
System.
Pump
speed
is limited to
28% when feedwater flow was
less
than or equal to 205.
The test run was reviewed
by the inspector while in progress
and
was determined
to be successful
in that the equipment
performed
well except for two problems.
They were:
(1) the cooling water
controller to
the
hydraulic oil heat
exchanger
on
the
hydraulic coupling did not control
in automatic
mode
and
was
manually operated,
and (2) The normal electrical
feeder breaker
for the
MG motor would not operate
which required the alternate
breaker to be in service for the operation.
Work requests
were
issued to correct the deficiencies.
d.
The
B recirculation
pump
was
run
on
March
28,
1991,
and
witnessed
by the inspector.
The
pump speed
was restricted
to
that of the
A
pump
and
the test
was
completed
without any
identified problems.
Reactor
Systems
Integrated
Cold Functional
This test,
2-BFN-RTP-ICF,
CN07, Integrated
Cold Functional,
was
performed
on April ll, 1991.
The test successfully
demonstrated
that the plant could
be cooled-down
and maintained
from outside
the main control
room if required during an accident situation.
This testing
was reviewed while in progress
by the inspector.
No deficiencies
were noted during the inspectors
review of the testing
activities.
~ ~
11
6.
Safety Parameter
Display System
(SPDS)
Following the event at TMI, operating reactor
licensees
were required to
install
a
to display to operating
personnel
a
minimum set of
parameters
defining the safety
status
of the plant.
Supplement
1 of
NUREG-0737 clarified eight
SPDS requirements.
The
NRR staff conducted
an audit at
BFN in November,
1990, to assess
the
status
of the
ISPDS with regard to the eight requirements
of NUREG-0737,
Supplement
1.
The staff concluded
that the
ISPDS
implemented for
Unit 2 satisfied six of the eight
SPDS requirements.
The two requirements
which were
not met were:
(1) provide rapid
and reliable aide
and
(2)
incorporate
accepted
human factors principles.
A third requirement
which
had not been
implemented at the time of the audit
was to have procedures
in place
and operators
trained with and without the
SPDS.
During this reporting period,
an inspector discussed
the open
issues
with
cognizant
licensee
personnel
and reviewed the
ISPDS in the Unit 2 control
room.
The
requirements,
NRR staff issues,
licensee
corrective
actions,
and the inspector's
findings were
as follows:
a ~
Requirement
- The
should rapidly and reliably aid the Control
Room operators
in determining the safety status of the plant.
Issue
1:
The software configuration
management
system
needs
to
be
formalized.
Action:
Issue
2:
Software
changes
on the
and plant process
computer are
controlled by section 3.15 of SSP-2.12,
Control of Computer
Application Software.
Software
changes
are initiated with
a "Software Services
Request"
which requires
review and
approval
from Nuclear
Engineering,
Information Services
Operations,
Technical
Support,
and other organizations
that
may be affected
by the change.
During the change
process
a
10 CFR 50.59 review and independent quality review are also
performed.
Some
touch screen
displays
and
keyboard function keys were
observed
to be unreliable
and must
be corrected.
Action:
Issue
3:
The function key problem
was
a result of a missing file on
the
terminal
which
was
repaired.
In addition,
developed
and
provided to
TYA a
touchscreen
calibration
program,
which
improves
the calibration
process.
Few
problems
have occurred since the
NRR audit.
Procedures
need
to
be
developed
for which
terminal
locations
and
personnel
can
make
ISPDS
software
and
database
changes.
12
Action:
The only terminal
that
can
make
software
and
data
base
changes
is located
in the
BFN computer
room.
Terminal
access
is controlled
by software
codes
and all software
changes
are
implemented
in accordance
with
TVA Nuclear
Standard
2. 12 and .BFN SSP-2. 12 (see
Issue I).
Issue 4:
Procedures
need
to
be
developed
to specify
how sensor
inputs with different scanning
rates
would be handled.
Action:
All sensors
on the currently installed
ISPDS have the
same
one
second
update
rate.
For the final
SPDS,
TVA will
ensure
that
a point is readily identified if it is scanned
at
a rate other than
a normal
update rate
by indicating in
the point description or point ID number.
b.
Requirement
- The
SPDS shall
be
designed
to incorporate
accepted
human factors principles.
Issue I:
The workstation
display for the
reactor
operator
had
excessive
glare from the control
room overhead lights.
Action:
The
CRT displays
were replaced with non-glare
CRTs.
Issue
2:
The
hood
on the
above workstation
obscures
part of the
ISPDS display (e.g.,
the
ISPDS parameter
summary box) when
an operator is in a standing position.
Action:
The hood was permanently
removed.
c.
Requirement - Procedures
should
be developed
and operators
trained
with and without the
SPDS available.
Issue:
Action:
At the time of the audit,
BFN Unit 2 operators
had received
only
a two-hour briefing on the operation of the
ISPDS.
The licensee
stated that operators
would be trained
on the
use of the
ISPDS during both the normal
EOI (i.e. without
the
SPDS)
and requalification training programs.
All operators
have
been
trained with and without
ISPDS.
Operator
training
without
ISPDS
is
accomplished
by
simulating failure of data
inputs
to the
ISPDS
during
training
on
the simulator.
In addition,
a feature
to
simulate failure of the computer which supplies
ISPDS data
has
been
installed
and
was
used
on the most recent
NRC
initial license
exams at
BFN.
Both of these
features
are
included in the training lesson
plans.
The inspector
concluded that all of the issues
identified by the
NRR audit
had
been satisfactorily
addressed
by the licensee.
No deficiencies
or
further concerns
were identified.
When
TVA declares
the full BFN Unit 2
SPDS operational
(during operating
cycle 7), the
NRR staff wi 11
issue
a
supplemental
safety evaluation.
~ ~
13
7.
System Pre-Operability Checklist (71707)
The inspectors
continued
to monitor the licensee's
activities to evaluate
and
upgrade
plant equipment
and documentation
as necessary
to insure that
plant systems
are in compliance with applicable
standards
and commitments
to support their required functions.
Those
systems
reviewed during this
reporting period are listed as follows:
a ~
b.
C ~
Service Air (System
33)
A walkdown of the major system
equipment
and completed
package
was
reviewed
by the inspector.
The
system
had required
extensive
maintenance
to meet to acceptable
standards.
Much of this
maintenance
was reviewed
by the inspector while in progress.
Only one deferral
remained
open which addressed
the quality level for
procurement
of consumables
utilized in the
system.
However, this
item has
been justified as not being
an operability issue.
All primary/critical drawings for the system
have
been
reviewed
and.
updated
as
appropriate
and
have
been
added
to the computer-aided
drafting program.
In addition, all drawing discrepancies
and design
change
notices
were reviewed
and
a determination
was
made there
were
none which would impact operability of the system.
No outstanding
deficiencies
were noted during the review that would
affect system operability.
Secondary
Containment,
System
64C
This system
was discussed
previously in IR 90-37.
The
SPOC for this
system
was
completed
on
December
10,
1990.
The inspector
reviewed
the
package
with the cognizant
system
engineer
and
noted that
three deferrals
and three exceptions
were issued.
The inspector also
noted that all the exceptions
and deferrals
had
been
closed.
No
deficiencies
were identified during the review of the
SPOC package.
The inspector also discussed
current
SMPL activities with the system
engineer.
The
inspector
noted that
there
were
several
actions
remaining
open for this
system;
however,
none
were
required
to
support the restart of Unit 2.
Off-gas
(System
66)
The inspector
reviewed the licensee's
completed
package of the
Off-Gas
System.
The
package
had identified
3 deferrals
taken for
items that could not be completed at the time of the
SPOC completion.
Two of the deferrals
involved testing that required the system to be
in operation to complete.
The third deferral
required replacement
of
4
RTDs that
was to be replaced
to meet design requirements.
Each of
the
3 deferrals
were evaluated
as not to affect system operability.
Oi
14
The inspector
had previously walked-down
the
system
and determined
that the equipment
appeared
to have
been well maintained.
However,
various
checkouts
were
performed
on the
system
which resulted
in
equipment,
instrumentation,
and electrical
components
being replaced
and/or modified.
This included,
but not limited to the replacement
of one of the mechanical
vacuum
pumps, electrical
cable for ampacity
problems,
pipe
and
tubing supports,
and
various
instruments
and
electrical
components.
In addition, the charcoal
absorbers
underwent
a dry-out/regeneration
activity to reduce
the moisture loading.
Based
on the review of the
system
and
Package,
there
were
no
remaining
open items determined
to prevent operation of the system.
Reactor Recirculation,
System
68
The
SPOC for this
system
was
completed
on
March
15,
1991.
An
inspector
accompanied
licensee
personnel
on the final walkdown for
this
system
on
January
24,
1991.
No major deficiencies
were
identified.
The
inspector
reviewed
the
package
with the
cognizant
system
engineer
and
noted
that
one
exception
and six
deferrals
were
issued.
The
exception
was
issued
to follow
replacement
of the recirculation
pump seals.
Replacement of the
pump
seals
has
been
completed
and
tested
during
the
reactor
vessel
test.
Four
of
the
deferrals
were
issued
for
modifications for which the field work was complete
but testing is
required for closure.
One deferral
was
issued for modifications
which were complete for system
68 but remained
open for work on other
systems.
The final deferral
was issued to follow blockage of the
811
jet
pump instrument line.
The instrument line was
unplugged
during
performance
of the
reactor
pressure
test
and
this
deferral
can
be closed.
No deficiencies
were identified during the
review of the
SPOC package.
Reactor
Core Isolation Cooling, System
71
The
SPOC for this
system
was
completed
on April 7, 1991.
The
inspector
reviewed
the checklist with the
system engineer
on April
11,
1991.
The
system
was
accepted
by the
plant staff with
5
deferrals
and
no exceptions.
The inspector
reviewed the list of
approved
deferrals
for
and did not note
any item that
was
significant or would affect system operability.
The
inspector
followed the
licensee's
activities
associated
with
testing of the
RCIC turbine
on several
occasions
during this
and the
preceding
reporting periods.
The licensee
has
conducted
a series of
special
operational
tests of the
RCIC turbine
on low pressure
steam
supplied
by the auxiliary steam
system.
This test
has
demonstrated
that the system is ready to support plant restart.
Reactor Protection
System,
System
99
The
SPOC for this
system
was
completed
on
December
26,
1990.
An
inspector
accompanied
licensee
personnel
on the final walkdown
on
0
15
g,
h.
December
14,
1990.
No major deficiencies
were identified.
The
inspector
reviewed
the
completed
package
with the cognizant
system engineer
and noted that four deferrals
were issued
against
the
SPOC.
Two of the deferrals
remain
open
pending
the completion of
testing.
One deferral
is
open for modification
on another
system
which is related
to system
99.
The final deferral
remains
open
pending
the closure of paperwork.
All deferrals
are scheduled for
completion prior to Unit 2 restart.
No deficiencies
were identified
during the review of the
SPOC package.
Buildings and Structures,
System
303
This
system
includes
those
various
safety
related
structures
associated
with the Reactor Building,
Control
Bay, Intake Structure,
Offgas Building, and
D/G Buildings.
The design
and construction of
these
structures
must
provide for mitigation of the effects of
tornado,
and flooding.
Although interior flooding is
considered
under
the
SPAE for this
system
most effects
associated,
with flooding from exterior sources
were covered
as part of the
for System 327, Flood Protection.
The system checklist
was
completed
on March 27,
1991.
The inspector
reviewed the
package with the system engineer
on April 15,
1991.
The
package
included
two deferrals
associated
with licensee
CAgRs which concerned
several
protective coating failures
and
use of
unqualified coatings
inside
the Unit
2 Drywell.
All field work
associated
with these
two
CAgRs
is
complete
and
the
remaining
activities not affecting system operability.
Carbon Dioxide and Fire Protection/Generator
Purge,
System
39
Containment Ventilation, System
64B
Radwaste
System,
System
77
The inspector
reviewed
and observed
the licensee's
activities in the
process.
These
observations
and
reviews
included
walkdowns,
review of punchlists,
and
PM.
Diesel Generator,
System
82
Additional reviews
were
performed
on
System
82.
This system
was
previously
SPOCed
and reviewed.
A TS change
was expected
and later
approved.
This change required that each
DG be tested at 2800
kw for
at least
24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
The licensee
commenced
these series of run tests
on March 18,
1991.
0
8.
Emergency Operating
Procedures
The
use
of the
BFN revision
3
versus
revision
4
has
been
reviewed
on several
occasions
by the
NRC staff.
During this reporting
period,
an inspector
reviewed
documentation
for EOIs
and
AOIs to verify
that the licensee
had completed
commitments
required for Unit 2 restart.
0
~ ~
16
a
~
In a letter dated January
18,
1990, the
NRC staff concluded that Unit
2 could
be safely restarted
using
the
BFN revision
3 EOIs.
This
letter contained
NRC staff
comments
on
6 items of concern.
reviewed
each of the comments
and submitted corrective actions to the
NRC by letter
on July 6,
1990.
The inspector
reviewed
the letters
and verified that the licensee
had implemented
the commitments.
The
issues,
responses,
and actions
taken were as follows:
Comment:
Guideline
PC/P,
Primary.
Containment
Pressure
Control, action PC/P-6. 1 is intended to prevent actuation of the
wetwell sprays if the nozzles
are
submerged.
Spray actuation
would result in water
from the nozzles
entering directly into
the
PSC.
The
have
taken
this action
when
the level
instrumentation
is at the maximum value.
For BFN, this limit is
20 feet while the nozzles
are at 26.4 feet.
This results
in a
space
of 6.4 feet where the sprays
could possibly
be effective,
but are not actuated
due to limitations of instrumentation.
(2)
(3)
TVA should
review alternate
methods
to determine level, rather
than limiting the actions
due to instrumentation limits.
Action:
The licensee
r'evised
PC/P to direct actuation of
sprays
based
on pressure
parameters
only.
Limitations based
on
level
were
removed
from the
procedure
at
steps
PC/P-2
and
PC/P-6.
Base
documents
were
also
revised
to support this
change.
Comment:
In general,
the
reason
for the action
given in the
EPGs in parentheses
is the basis for the action.
However, the
have also triggered actions
due to instrument limitations
as indicated in (1) above.
If the action is based
on instrument
limits, it should
be so stated.
Action:
The
EOIs were reviewed to ensure
that actions
taken
based
on instrument limits reflect that the instrument
range
limitations is the basis for the action.
Guidelines
PC/P-2
and
PC/P-6 were revised
as described
in (I) above.
Comment:
The draft that
the staff
reviewed
had
several
inconsistent referrals.
For example,
PSC water level
was given
in negative
inches
from normal
as well as
a measurement
in feet
from an absolute reference.
Also, the wetwell is referred to as
as well
as the wetwell.
Special
note
should
be taken to eliminate these
types of inconsistencies.
Action:
TVA agreed
that
inconsistent
referrals
should
be
eliminated.
In the first example
given, the inconsistency
is
necessary
due
to the
need
to
use
narrow-range
rather
than
wide-range instrumentation for determining
PSC water level.
The
narrow-range
instrument
has
a different zero reference
point,
with zero
being
normal level,
and
reads
in inches rather
than
feet.
I
0
Cl
0
17
The EOIs were reviewed to ensure
consistency
in the use of terms
concerning
primary
containment,
drywell,
and
PSC.
No
inconsistencies
were found in the procedure.
The program manual
was revised to include definitions for all terms
used to signify
components of primary containment.
Comment:
The actions
indicate
there
is
no manual
action to
initiate either the
RHR or
CS room coolers.
This limitation is
not normal for a Mark I design
and should
be verified before the
option is discarded.
Action:
The
RHR and
CS equipment
area coolers
are not provided
with manual start capability.
The cooler fans
auto start
on
a
corresponding
pump start or increasing
temperature
(100
F) in
the
immediate
area.
Control
Room indicators
are provided for
monitoring
pump
room temperatures
and annunciators
are provided
to alert operators
of cooler failure at
150 F.
The option to place
jumpers at the
room cooler circuit breakers
in the
RMOV boards
was reviewed.
This option was considered
to
be unfavorable
when weighing the capacity of the coolers
and the
adequacy
of existing cohtrols
and instrumentation
against
the
necessity
to dedicate
personnel
to this task
under
accident
conditions.
Comment:
Several
actions
in EOI-3, Secondary
Containment
and
Radioactive
Release
Control,
are
based
on the operator
being
able determine
whether the pipe rupture is within the primary or
secondary
system.
However, there is no guidance
provided to the
operator
in determining
which system
is affected.
This is
a
deviation
from the
symptom
based
EOIs since it requires
an
evaluation
by the operator.
The
should
provide
some
guidance
on how an operator should determine
the break location.
Action:
EOI-3 was revised to provide guidance
to the operator
for determining
break location.
Comment:
EOI Guideline
RC/P,
Pressure
Control, contingency
C2,
Emergency
Depressurization,
is entered if reactor
water level
cannot
be determined.
However, in the
BWROG revision
3 EOIs,
the appropriate
action is flooding the
RPV when reactor water
level
cannot
be
determined.
TVA committed
to revise this
procedure to reflect
BWROG guidance.
Action:
Previously,
in the
C2 was entered if reactor
water
level could not
be determined.
After depressurization,
C4,
RPV Flooding,
was
then entered.
TVA revised EOI-1, Reactor
Control,
to require
entry into
C4
when
RPV level
cannot
be
determined,
rather than enter
C2.
0
18
b.
In
a letter dated
October
16,
1989,
the
TVA made
two commitments to
improve
and
AOIs for Unit
2 restart.
The inspector
reviewed
documentation
and verified that the actions
had
been
completed.
No
deficiencies
were identified.
The commitments
and actions
taken were
as follows:
(1)
Commitment:
Develop
and
include
additional
information for
hydrogen control in an AOI which references
EOI-2.
Action:
Procedure
2-A01-64-8, Primary. Containment
High Hydrogen
and/or
was issued
on June
1,
1990, to provide
symptoms
and operator actions f'r control of combustible
gases
or Oxygen) in the primary containment.
(2)
Commitment:
BFN will have
a method
in place
to provide
an
alternate
means of injecting boron following a failure to scram.
Action:
Procedure
1-SOI-26,
Use of U-1
SLC Storage
Tank
As An
Alternate Source of SLC Injection For U-2, was issued
on January
10,
1990,
to maintain the Unit
1
SLC system
tank available for
injection into the Unit 2 reactor
vessel
by using
the
1B
system
pump.
This
method
is
included
in
Appendix
2,
Alternate
SLC Injection.
c.
As part of the procedure
upgrade
program committed to in Volume 3 of
the
NPP, all AOIs were to be upgraded
and verified prior to Unit 2
restart.
The verification process
for AOIs includes
an in plant
walkdown to verify that the instruction will work and obtain operator
comments.
The backup control
room provides
a means for operators
to safely shut
down the reactor
from outside of the main control
room in the event
of
a main control
room evacuation.
Procedure
2-AOI-100-2, Control
Room Abandonment,
provides
instructions for Unit 2.
The inspector
reviewed the AOI to verify that comments
from the plant walkdown were
incorporated
into the instruction.
The
walkdown
was
conducted
by
Operations
personnel
in October,
1990.
The inspector
noted that most
of the
comments
involved equipment
labeling
and procedure clarity.
The
inspector
reviewed
the
walkdown
comments
against
the current
revision of the AOI (rev. 7) and noted that appropriate
comments
were
incorporated.
The inspector identified
a few typographical
errors to
Operations
personnel
who
issued
procedure
changes.
No further
deficiencies
or inspector
concerns
were identified.
9.
Nuclear Instrumentation Reliability
Browns Ferry has
had
a history of poor reliability associated
with System
92,
Nuclear
Instrumentation.
As part of the
process
the
system
checklist for System
92 was
completed
on August 27,
1990.
This activity
was monitored
by the inspectors
as
documented
in inspection reports
90-25
and 90-27.
The system
was accepted
by plant staff with a relatively high
number of exceptions
and deferrals
compared
to other system
This
19
was mostly due to
a large
amount of unfinished work activities that were
needed
to support
system operability.
These
in'eluded
replacement
of ll
defective
LPRM strings
and repair or replacement
of various
undervessel
cables.
Various work on the
NIs
was
ongoing until just before fuel load.
The
licensee
initiated core reloading activities
on February
21,
1991, while
experiencing
problems
with
SRM Channel
B.
The
sensor
input to this
channel
was
from
a
FLC which is
more sensitive
than
the
normal
detectors.
A later licensee
investigation
determined
that the excessive
noise resulted
from damaged
connectors
was
a contributing factor to this
problem.
The
IRM gain
adjustments
were set to
maximum
by 2-TI-233 the
weekend
before fuel load.
Just prior to fuel load the range
switches
were set
down to position
1 (the lowest position).
Noise
was evident
on the
channels
with channel
readings
remaining
above
downscale
throughout fuel
loading.
There
was
no noticeable
correlation
between
channel
indication
and fuel bundle addition.
Since fuel
load
was
completed
the licensee
has
experienced
many nuclear
instrumentation
spikes
and
spurioUs
RPS trips.
Some of the spikes
were
severe
to cause
a channel
Hi-Hi alarm but not of sufficient duration to
pick
up
a
relay
and
cause
a halfscram.
Most of this erratic
indication could readily
be attributed to noise
and faulty
IRM signals
that could result
from various
causes
such
as
grounding
problems,
bad
connectors,
cable crosstalk or inductive cable coupling.
was
contacted
and
arrangements
made
for
a visit by
a
vendor
representative
from GE's office in
San
Jose
to travel to the site to
assist
in the troubleshooting effort.
Based
on their review
GE made the
following test methodology recommendations:
Measurements
of shield to ground resistance,
signal to noise ratio,
and capacitance
to check the transmission
path from the detectors.
Verification of proper
impedance
values for channel
cable,
connector
and detectors.
Connection
of
a
recorder
with adequate
"response
to selected
channels
to allow recording of spike amplitude.
This data to be used
for accurate
baseline
data.
Licensee
should diagnose
SRM,
IRM,
LPRM channels
with known spiking
problems to determine
location of problems.
Concentrate
on channels
which shown inoperative
by analysis of cable data.
After adequate
date is obtained,
the licensee
should readjust
the
gain
on the
IRMs to an
optimum value (reduction in gain could mask
the noise
and
make troubleshooting
more difficult).
t
20
The
inspectors
followed the
progress
of the licensee's
troubleshooting
activities
in this
area.
A description
of activities
observed
is
described
in paragraph
2.a.
During his visit the vendor also
showed the
licensee
better
ways to acquire
low current measurements
for data taking
and
newer connector
cleaning techniques.
The troubleshooting activities
on the NIs had to be halted
on April 22,
1991,
due to scheduled
work under
the Unit
2 reactor
vessel
to replace
the leaking
CRD Mechanism 0-rings
that
had
been identified during the
RPV hydro.
NI troubleshooting
is
scheduled
to
resume
when the 0-ring replacement
work is completed.
personnel
in San Jose
are presently working on procedures
to assist
TVA in
further testing
and
setup of the nuclear instrumentation.
They plan to
complete this effort in time to allow returning to the site for the second
stage
of troubleshooting.
The inspectors will follow the licensee's
actions in this area during the next reporting period.
10.
TMI Action Items
a.
(CLOSED)
260/TMI Action Item II.E.4.2. 1-4,
Containment
Isolation
Dependability - Implement.
Related
to this item was
BU-80-06,
Engineered
Safety Feature
Reset
Controls,
which was closed ia
IR 90-40.
The
NRC issued
TS Amendment
No.
193 on March 22,
1991.
This was
a review of 10 CFR 50 Appendix J
and TMI Item II.E.4.2.1-4.
The
SE concluded that TVA identified each
containment
system for Unit 2 as essential
or non-essential,
assured
that all essential
systems
were
remote-manually
operated
and
the
non-essential
systems
met
the
intent of isolation
requirements
specified in General
Design Criteria of 10 CFR Part 50, Appendix A.
Additionally,
a
successful
integrated
containment
leak
rate
inspection
was
completed
on
March
18,
1991.
These
reviews
and
inspection close this item.
b.
(CLOSED)
260/TMI Action Item II.F.2, Instrumentation
for Detection
of Inadequate
Core Cooling.
This item evolved from the Three Mile Island Incident and
addressed
the
need for additional
instrumentation
or controls
to supplement
existing instrumentation
to provide
an unambiguous,
easy-to-interpret
indication of inadequate
core cooling.
Two categories
of permanent
physical
improvements
were identified in Generic Letter
No. 84-23
which provided
BWRs with clarification of
NRC requirements
in this
area.
The two required areas of improvement are
as follows:
Improvements
to plant design that will reduce level indication
errors
caused
by high drywell temperature.
Review of plant experience
about
mechanical
level indication
equipment.
Evaluation
of
any existing
mechanical
level
indication for replacement with analog level transmitters.
21
The
inspector
reviewed
documentation
provided
by the
licensee
to
support
closure of this
TMI Action Item.
During this review the
inspector
determined
that the licensee
had adequately
addressed
this
issue
to support closure of the item.
Specifically the
inspector
determined
the following:
P7131
rerouted
the Unit
2 reactor
water level
reference
legs,
to minimize the routing of the reference
legs
inside the
drywell.
The resident staff followed the
progress
of this
modification
including
performing
a
walkdown of the
work
activities.
This
inspection activity was
documented
in
IR
88-32.
This
ECN is
now field complete with the cold functional
portion of the post modification testing
completed.
The only
remaining testing that is not complete is the hot functional
testing of water level instrumentation
which must
be performed
after restart
during
power
ascension
testing.
An inspector
reviewed
the completed modifications work package
and observed
portions of 'the requalification training for licensed
operators
on this subject.
The licensee
replaced substantially all mechanical
reactor water
level indicators for Unit 2 during the performance of ECN P0126.
This modification is field complete.
The inspector
determined
there
are still
two existing
Yaryay
type
water
level
instruments,
2-LI-3-46A and
2-LI-3-46B, which provide
water
level
indication at local
instrument
racks
and at the
remote
shutdown
panel,
2-25-32.
Although these
two instruments
are
mechanical
type level
instrumentation
all Unit 2 water level
instruments
that initiate Reactor Protection
and
ECCS functions
and
provide
level
indication in the control
room
have
been
replaced
with analog
type
instrumentation.
An inspector
observed
portions of the work activities associated
with this
modification
and
attended
a portion of the requalification
training for licensed operators
on this subject.
The staff
had
reviewed
the
above
proposed
modifications
and
determined that both modifications were acceptable
to address
the two
improvement categories.
That review is
documented
in NRC's letter
dated
November
18,
1986.
During the
above
reviews
the inspector verified that the completed
modifications activities were accomplished
by the licensee's
approved
design
change
process.
The licensee
has
adequately
implemented all
improvements identified in the licensee's
responses
to
GL 84-23 dated
April 8,
1985, July 15,
1985,
October
15,
1985,
and March 12,
1986.
Additionally this
satisfies
the
commitment
to
complete
all
Item II.F.2 related modifications prior to restart of the
unit identified in TVA letters
dated
March 1,
1988,
and October
18,
1988.
r
0
22
The inspectors will continue
to monitor licensee activities in the
area
of reactor
vessel
water
level
including followup of any
abnormalities
such
as
level
mismatch.
This will also
include
followup of licensee activities to address
IFI 259, 260, 296/89-35-01
which although not
a restart
item should
be resolved during the power
ascension
testing
program prior to full power operation.
(CLOSED) 260/TMI Item II.K.3.18.C,
ADS Logic.
Previous
inspection
reports
documented
reviews of this item.
The
outstanding
work activity
required
was
the
performance
of
PMTP-BF-.01.014.
The
post
modification test
was
successfully
completed
on March 22,
1991.
In addition to
a review of the
PMTP the inspector
also reviewed the
following procedure:
2-SI-4.2.8-1,
Core
and
Containment
Cooling
Systems
Reactor
Water
Level
Instrument
Channel
Calibration;
2-SI-4.2.B-ATU,
Core
and
Containment
Cooling Systems
Analog Trip
Unit Functional
Test;
2-ARP-3C, Alarm Response;
and 2-EOI-1, Reactor
Control,
Section
RC/C, Monitor and
Control
RPV Water Level.
The
inspector
also
discussed
this
item with licensee
representatives.
Based
on
the observations,
reviews,
and discussions
the inspector
concluded that this item was implemented.
(CLOSED)
260/TMI Action
Item II.K.3.27,
Common
Vessel
Level
Reference.
The licensee notified the
NRC in a letter dated
March 14,
1991, that
TMI Action Item II.K.3.27, and
Human Engineering
Discrepancy
HED 283
were
completed.
The
design
had
been
finalized,
modifications
completed,
procedures
issued
and the
necessary
training completed.
The inspector
reviewed
the licensee
closure
package for this item.
TS Amendment
157 was issued
November 28,
1988 and changed
the reactor
water level zero reference
point from the top of active fuel to the
bottom of the reactor vessel.
Documented
in IR 90-40
was
the results
of a
NRC audit
team which
concluded that all restart
HEDs including
HED 283 were satisfactorily
implemented.
Plant
DCN
W10396A replaced
the existing
scales
on
2-LT-3-52, 620, 2-LR-3-62 and 2-LIS-3-52,
62A in the control
room and
auxiliary instrument
room to reference
instrument zero
equal
to 528
inches reactor vessel
inside height.
The inspector
concluded
the TMI
Action Item had been resolved.
(CLOSED) 260/TMI Item II.K.3.28, ADS Accumulator gualification.
In
previous
inspections
the
inspector
documented
reviews
and
observations
involving this
issue.
The
inspector
reviewed
the
following procedures:
2-0I-84,
Containment
Atmosphere
Dilution
System
Operating Instructions,
2-0I-32A, Drywell Control Air System
23
Operating Instructions,
and 2-AOI-32A-1, Loss of Drywell Control Air.
In
addition,
the
inspector
held
discussions
with
licensee
representatives
involving the modification to Systems
84,
CAD and 32,
DCA.
One item remained
open
and involved containment isolation valves in
Systems
32
and 84.
TVA decided
to replace
the Unit 2 outboard
check
valve
in
each
train with
a qualified
normally closed
solenoid
valve
and
a normally closed
manual
valve,
which bypasses
the solenoid
valve, prior to restart
from the next
refueling outage,
Unit 2, cycle 6.
Based
on the reviews,
observations,
and discussions
the inspector
concluded
that this
TMI Action Item was adequately
implemented for
Unit 2, cycle 5.
11.
Information Notice
Previously Unidentified Release
Path
From
Boiling Water Reactor
Control
Rod Hydraulic Units,
was
issued
to alert
licensees
of
a potential
accident
that could
to
a design
basis
accident with radiation
doses significantly exceeding
the values specified
in the
FSAR.
The accident
scenario
involves
a release
path in the
system
resulting
from
a break in the non-seismic
portion of the water
supply line to the suction of the
CRD pumps at
a time one of the
CRD pumps
is not in operation.
The portion of the referenced
piping is that located
outside the secondary
containment
boundary where
a line break could result
in the path of radiation release.
The licensee
reviewed
the
IN and determined
that stop
are
installed
in the
BFN system at the discharge
of the
pumps
which would
prevent
a backflow through the system to those portions of piping system.
Although these
stop check valves
have
been leak-rate
tested
and found to
have very minor leakage rates,
they are not part of the
ASME, Section
XI
Testing
Program.
However,
the
licensee
has
internally committed to
include
these
check
valves
in the
program prior to the Unit 2, refuel
cycle 6.
12.
Reportable
Occurrences
(92700)
The
LERs listed
below
were
reviewed
to determine if the information
provided
met
NRC
requirements.
The
determinations
included
the
verification of compliance
with
TS
and
regulatory
requirements,
and
addressed
the
adequacy
of the event description,
the corrective actions
taken,
the
existence
of potential
generic
problems,
compliance
with
reporting
requirements,
and
the relative
safety
significance
of each
event.
Additional in-plant reviews
and discussions
with plant personnel,
as appropriate,
were conducted.
a.
(CLOSED - Unit
2
ONLY)
Design of Suppression
Pool
Vacuum Relief System
Does
Not Provide
Single Failure
Double
Isolation of Primary Containment.
~
~
0
24
This was
a voluntary
LER which addressed
the possible failure of the
suppression
pool
vacuum relief system in the open position
on loss of
its unqualified air supply.
This did not meet
the current single
failure double
isolation
design criteria for primary containment
integrity, identified in Generic Letter 88-14.
DCN W14096A
was
implemented
to provide
CAD system nitrogen at the required
pressure
to the
vacuum breaker butterfly valves if the normal air supply from
the control air system is unavailable.
The inspector
reviewed the
closure
package
for this
item
and
the applicable
DCN.
This
DCN
addressed
the concern
and
has
been
completed for Unit 2.
'CLOSED)
Residual
Heat Service
Water
(RHRSW)
Pump
Auto-Start
Problem Following an
Unplanned
Engineered
Safety
Feature
Actuation.
Between
the
dates
of August
28-30,
1990
plant modifications
electricians
replaced
time delay relay
TD2A and installed
a
new test
block in the control circuit of RHRSW
pump
A3 under
DCN W4515A.
At
the
completion
of this work,
no
was
immediately
performed.
Although one of the "General
Requirements"
contained
in step
6.1 of
SDSP-14.9
requires
that caution orders
be established
for components
awaiting
PNT and that
a caution order
tag
be
hung at each control
location from which that component
can
be operated,
the inspector's
followup of this event disclosed
that
no such caution order tag was
issued for RHRSW pump A3.
'n October
4,
1990
pump
A3 was lined
up to supply
an
and
"assigned"
per
step
7.8 of 3-SI-4.9.A.1.a(3D)
to
automatically start following the start of the
3D diesel
generator.
Pump
A3 failed to start.
During the inspector's
followup of this
event, it was noticed that the
same
A3
RHRSW pump had also failed to
autostart
a few days earlier during the monthly operability test of
the
3C diesel
generator
performed via 3-SI-4.9.A.1.a(3C)
on September
27,
1990.
This September
27,
1990, failure then resulted
in the
issuance of TD-1 and
WR O'C-039315
(and associated
WO 890-18430-00).
Since the cause of its September
27,
1990, failure to start
was still
unknown
and the associated
corrective action
documents (i.e.
TD and
WO) remained
open at the time, the assignment of the A3
RHRSW pump to
autostart for the
performance
of the October 4,
1990,
SI test
was
incorrect.
This test
control
inadequacy
resulted
in incomplete
compliance
with all the requirements
of plant procedure
PNI-17.1,
Conduct of Testing.
Trouble shooting activities
on the
A3
pump completed after its
October 4,
1990, autostart failure, resulted
in the discovery that
a
wire not terminated
on terminal
8 of auxiliary relay
NVA-Al was
responsible
for the failure.
This lifted lead provides
the coil
current to time delay relay TD2A.
Failure to terminate this wire was
attributed
by
the
licensee
to
personnel
error
during
the
implementation of DCN W4515A.
25
The Dl
pump which was not aligned (i.e. its discharge
valve to
the
EECW system
was closed
even
though the licensed unit operator
on
shift had circled the "assigned"
option for RHRSW pump Dl in the
same
step 7.8 referenced
above
) to respond
to the diesel
generator start
signal, automatically started resulting in an unplanned
actuation of
an
ESF.
During
subsequent
trouble
shooting
of the
Dl
pump start
interlock circuit, the licensee
was unable to identify or duplicate
the cause of the failure that resulted
in the incorrect
pump start.
An improperly fitting relay cover suspected
to be associated
with the
unexpected
pump start
was
removed
from auxiliary relay RI located in
junction box 4860 under work order 90-20209-00
on October 25,
1990.
The absence
of a caution order tag
on the control switch for the A3
pump in addition to the inadequate
review of open corrective
action
documents
are test control
inadequacies
which permitted the
incorrect assignment
of the
A3
RHRSW pump to autostart
on October 4,
1990.
This is
the
second
example
of
VIO 259,260,296/91-10-03,
Inadequate
Test Control.
Any further inspector
followup of the circumstances
associated
with
this
event will be
performed
during followup of the licensee's
corrective action for the violation.
(CLOSED)
Failure to Establish
Hourly Firewatch
in
the
Required
Timeframe
Necessary
to Meet Technical
Specification
Requirements
for Inoperable
Fire Detection Panels.
On December
12,
1990,
TS 3. ll.A associated
with compensatory
measures
for inoperable fire detection
equipment
was
not met in that the
required
hourly firewatches
were not established
within one
hour.
The failure occurred
when the
1A ILC Bus tripped resulting in a loss
of electrical
power to various fire protection
system fire detection
panels.
Licensee
personnel
attempted
to establish
compensatory fire
watches
within the required
time frame.
However
a lack of clear
guidance for watch areas
in plant procedures
resulted in that process
requiring more that one hour to complete.
The inspector
reviewed
the licensee's
submittal for this event
and
determined
that it met current
NRC requirements
for reporting.
Additionally the
inspector
noted
that
two other similar events
occurred
during
the
same
period
(December,
1990).
These
two
additional
events
are
documented
in
LERs
259/90-17
and
259/90-21.
However this event
had
a different root cause
in that it resulted
from lack of procedural
guidance
which required different corrective
actions.
As corrective action to this event the licensee
developed
a
list of affected
areas for each of the three units.
This list was
issued
as
Operations
Standing
Order
OS-0023
and
was
made effective
March 8,
1991.
Based
on the
above review the inspector
determined
26
that
the
licensee's
actions
should
be
adequate
to
preclude
recurrence.
(CLOSED)
Rev. 1,
Actuation
During
Relay
Testing
Caused
by Procedure
Inadequacy
and Personnel
Error.
This event occurred
December
14,
1990, during the performance of a
time delay relay setpoint
check for the fuel
pool cooling
pump
1B
motor.
The
power source for the synchronous
timer used
to test the
relay was obtained
from 480V shutdown
board. 1B breaker control
power.
The
of the timer were attached
to the terminals
across
the
shutdown
board's
breaker control transfer switch.
The normal feeder
breaker for the
480V shutdown
board
1B tripped
when the timer was
energized.
The
deenergization
of this
shutdown
board
in turn
deenergized
bus
1B and the
PCIS logic relays
powered
by the bus,
resulting
in the isolation of group
2 valves
(drywell floor and
equipment drains discharge
valves).
The inspector
reviewed the licensee's
closure
package for this
LRED.
The licensee
attributed
the root cause
of the event to procedural
inadequacy
and
personnel
error.
Personnel
involved received
a
written warning.
The
EMI wi.ll be revised to require
a portable
power supply for time delay relay setpoint checks.
A portable
power
supply will be procured
by May 31,
1991.
(CLOSED for Unit
1
and
2 only)
Failure of
Two
Trains of the Standby
Power System to Load Sequence
Thereby Creating
the Potential for a Loss of Critical Safety Functions
On
December
27,
1990,
during
the
performance
of
"A" load
acceptance
test,
the
shutdown
board
"A" DGVA relays failed to stay
energized.
On
December
31,
1990, during the performance
of
DG "D"
load acceptance
test,
the
shutdown
board
"D" DGVA relays failed to
energize.
The
licensee
initiated
CA(R
BFP-910004
on
January
2,
1991
and
subsequently
issued
report II-B-91-004 to formally address
the cause
of these failures.
Based
on their
investigation
of the
circumstances,
the
licensee
concluded
that malfunctions in the operation of certain contacts
on
the stationary auxiliary switches
located
inside
each of the diesel
generator
breaker
cubicles
were
responsible
for the
observed
anomalies.
Closure of these
contacts
is required for energizing the
DGVA relays
which is
a prerequisite for the proper sequencing
of the
ECCS loads
and for the initiation of the load shedding logic when
an
accident
signal is present.
Consequently,
any inadvertent
premature
reopening
or failure to close of these stationary auxiliary switch
contacts
is undesirable
from
an
ECCS availability standpoint.
A
simultaneous
combination of the events
that occurred
December
27,
1990
and
December
31,
1990 could have resulted
in a failure of both
27
pumps
to start, resulting in the potential
loss of both
loops of a critical safety function.
To ensure
the
DGVA relays energize correctly,
a redundant
and diverse
contact,
located
on the breaker
mounted auxiliary switches
of the
diesel
generator
output breakers,
has
been installed in parallel with
the contacts
on the existing stationary auxiliary switches for the
Unit
1
and
Unit
2
shutdown
boards.
A similar design
has
been
implemented
for
the
NVA relays
which could also initiate
load
sequencing.
A similar modification for the
Unit
3
shutdown
boards will be
implemented prior to the Unit 3 startup.
In addition,
on
March
28,
1991,
the
licensee
initiated
a
change
request
to procedure
EPI-O-OOO-BKR002,
"Maintenance
of
(Magne-
Blast)
Switchgear
and Circuit Breakers"
which will require
a visual
inspection
of the stationary auxiliary switch contacts
during the
once per outage
breaker inspections.
Any further inspector followup of these
ESF testing deficiencies will
be conducted
during the followup of unresolved
item
URI 259,
260,
296/90-40-01.
This
LER is closed for Units
1 and 2.
(CLOSED)
Deenergization
of
Reactor
Protection
System
Bus
by Normal
Supply Circuit Protector
Operations
Caused
by
Failure of Overvoltage
Voltage Monitor.
A February
1, 1991, trip of the
3A2 circuit protector resulted
in
the deenergization
of the
120 volt 3A
RPS distribution bus.
The
circuit protector trip occurred
because
of a faulty internal voltage
monitor used to sense
supply overvoltage.
The deenergizing of the
3A
RPS distribution bus resulted in an unplanned
actuation of engineered
safety features.
The
systems
affected
by this actuation
were the
Unit
3
Primary
Containment
Isolation
system,
the
Standby
Gas
Treatment
system,
the Control
Room Emergency Ventilation system
and
the Unit 3 Reactor
and
unit-common
Refuel
zones
normal ventilation
systems.
The licensee
issued
IIR No. B-91-030
on February
11,
1991.
Random
component failure of the
3A2 circuit protector
was identified as the
root cause of the event.
A new overvoltage relay was installed under
work order
891-25966-00
and its associated
post-maintenance
testing
per procedure
3-SI-4.1.B-16,
"RPS Circuit Protector Calibration/FT"
was completed
on February 2,
1991.
The defective voltage monitor is being returned to the vendor for an
evaluation
of the failure.
The licensee
is also evaluating
the
availability of substitute
class
1E voltage monitoring hardware for
possible
replacement
of the existing
monitors.
The
inspector
determined that the licensee's
evaluation of this event
was adequate.
~y
28
13.
Action on Previous
Inspection
Findings
(92701,
92702)
a
~
(CLOSED)
IFI
260/87-09-05,
Final
Resolution
of
Unverified
Portions of CCD Drawings.
This issue
was previously'reviewed
in IR 88-33
and
IR 91-02.
The
results
of those
reviews
were that this item was resolved for fuel
load, but
NRC review of audit reports,
CAgRs,
and schedules
for CCD
implementation
were necessary
to close this item for Unit 2 restart.
During this reporting period,
an inspector
reviewed licensee
audits
which involved
reviews of plant design
bases
and
design
control
issues,
including CCDs.
The reports
reviewed were
EA Audit BFT89901
"Design
Change Control",
N(AEE Audit BFA89003 "Technical
Evaluation
of the
RHR System",
and
NgASE Audit BFA90022
"BFN Configuration
Control
and
SPOC/SPAE
Process."
The inspector
noted that the audits
contained
several
examples
of drawing inconsistencies;
however,
no
problems
were identified involving unverified portions of CCDs.
The
problems
identified in the audits
reviewed
were dispositioned
by
approved
plant
procedures.
Drawing
inconsistencies
are
being
followed by other
NRC open items.
From
discussions
held
with cognizant
licensee
personnel,
the
inspector
found that there
were
358
CCDs
completed
and
260
CCDs
remaining to be completed
as of March 19,
1991.
The remaining
CCDs
must
be completed prior to Unit 2 restart.
The inspector
concluded
that
the
licensee
was
implementing
a
program
to
document
the
evaluated
plant configuration of the portions of systems
within the
safe
shutdown
boundaries.
This is in accordance
with the licensee
commitment
for the
Phase
I
DBVP.
No further
concerns
were
identified.
b.
(CLOSED)
IFI
50-260/89-16-09,
Need
to
Consider
Flow
Degradation
Due to Corrosion of Carbon Steel
Piping.
This issue
was identified during the
VSR inspection of the
CS system
and
documented
in IR 50-260/89-16.
The team identified that for all
calculations
involving the determination of a system
pressure
drop,
the
method
used
did not account for an
increase
in the relative
roughness
of the pipe inside surface
as the pipe
ages (i.e.,
due to
corrosion
or
other
causes.)
Specifically,
calculations
MD-f2075-87215,
Revision 0,
"Pipe Sizing of Core Spray System,"
and
MD-(2075-87258,
Revision
1,
Pump
and
Performance
Calculation" did not account for the aging effect
on carbon
steel
piping.
After the initial inspection,
the
licensee
provided
additional
information regarding
flow degradation
due to corrosion of carbon
steel
piping.
This additional
information indicated that other
architect-engineering
f'irms and utilities contacted
by TVA also
do
not assume
flow loss from carbon steel
piping corrosion
on condensate
or feed
system.
The licensee
agreed
to reevaluate it's position
on
the
need
to
assume
flow loss
because
of recent
information
from
J
~
0
29
industry that indicated that corrosion
may have contributed to system
flow loss at other utilities.
During this inspection
TVA provided
the following information
and
position:
TVA has
re-evaluated
the information submitted
to the
NRC
as
follow-up to the
VSR question
on flow degradation
of carbon
steel
piping.
TVA reaffirms its original position
on flow
losses
from degradation
of carbon
steel
pipe
when performing
pressure
drop calculations.
Degradation of carbon steel
pipe in
chemically treated
water
systems
is not
a factor which will
adversely affect pressure
loss.
Any corrosion which may occur
would be
a smooth black iron oxide film, passive
in nature,
and
would retard further corrosion.
This type of corrosion
is
consistent
with
the
roughness
factors
utilized
in
the
calculation.
The
main
component
which controls
the rate of
corrosion
in condensate/feedwater
systems
is dissolved
content.
BFNP conforms
to the
GE guidelines for this element
and
has experienced
no degradation of systems
in which the water
chemistry conforms to these
GE guidelines.
TVA has
evaluated
information received
on the
H.
B.
Robinson
auxiliary feedwater suction line problem and determined that the
corrosive condition described
is not relevant to the
CS system
steel
piping at
BFNP.
The
H.
B.
Robinson auxiliary
suction line was susceptible
to introduction of raw
water
which could greatly accelerate
the corrosion
process.
That type of condition cannot
be developed at
BFNP since the
system
piping is normally charged with condensate
grade water.
During outages
the
system
may
be drained for maintenance,
but
there
has
not
been
any evidence
of accelerated
corrosion or
roughness.
The Core Spray System cannot
be directly aligned to
a
raw water
system
to allow the introduction of water
not
chemically and/or mechanically treated.
Thus,
TVA's original position
and methodology in the pressure
drop calculations
are appropriate.
The inspector
reviewed the information provided
by the licensee
and
reviewed the effects of roughness
on head loss.
The crane technical
paper
410; flow of fluid through valves, fittings and pipe
was used
for this
review.
The effects
of pipe wall
roughness
in the
calculation
is relatively small
when
compared
to. other
head
loss
factors.
The overall effect of roughness
is only 2 - 3 percent
and
if a slightly higher relative roughness
ration
E/D is used it would
have little effect.
Additionally,
GE indicated that the
20 percent
head
loss
value
used
on the
process
drawing
was for pump sizing
calculations
and
should
not
be interpreted
as
being
a
surface
degradation
requirement
on this system.
30
(CLOSED)
IFI
259,
260,
296/89-49-01,
Maintenance
Activities
Involving Rework, Repair, Use-As-Is.
This item was identified during
a significant review of maintenance
activities.
The activity was originally associated
with insulation
required for freeze
protection
and
was
expanded
to include other
activities.
The concern
involved maintenance
personnel
restoring
a
system
impacted
by significant maintenance
to a configuration not in
keeping with design.
The inspector
observed activities,
reviewed
records,
and
spoke
with several
licensee
personnel.
From these
observations
and
reviews,
the
inspector
determined
that
when
maintenance
personnel
are restoring
a system following significant
maintenance
no
unauthorized
parts,
circuit modifications
or
insulation
can
be installed without a deliberate
act of not following
procedures.
In the case of spare parts,
no shop spares
are utilized
and this
includes
fasteners.
All parts
are
maintained
in the
warehouse
and
have
PEG involvement when
a replacement
is required.
(CLOSED) IFI 260/90-29-02,
Leaking Drywell Penetrations.
During
a final walkdown of the
RWCU system
two drywell penetration
was
observed
to
have
been
leaking.
The inspector
reviewed
the
licensee's
closure
package for this item.
and
902266800
were written to inspect,
clean,
and repaint penetration
2
X
15
and
2
X 28.
Both of the penetrations
were
checked for leaks
during the ILRT.
No leaks were identified.
(CLOSED) IFI 260/90-36-01,
Inadequate
Vendor Source
Inspection.
This item was identified by the inspector of record
when
a review of
source
surveillance
records
disclosed
that
TVA contract
no.
the materials
and
procurement
quality surveillance
report
W43901107-219,
dated
October
25,
1990,
stated
that
the
manufacturer's
conformance
to process
and materials of construction
could not be verified because
the items
under contract
were
made at
another
manufacturing plant.
The items involved were identified as
non gA, pressure controller parts (flapper and nozzle)
procured
under
purchase
order number 25-13360 from Controls Southern
Inc.
The parts
manufacturer
was identified
as
Fisher Service
Company of Columbia,
South
Carolina,
and
the
place
of manufacture
was
one of this
company's
plants
located in Marshall
Town,
Iowa.
The problems
were
created
when
TVA's vendor
inspector
failed to
communicated
his
inability to verify the surveillance
plan attributes with management
and engineering.
This communications
breakdown allowed the material
to
be approved for shipment to the site.
Following the disclosure
and the subsequent
issuance
of CARR no.
BFP900375,
dated
December
12,
1990,
the material
in question
was
surplused
by the
licensee.
Corrective actions
taken to prevent recurrence
included instructions
31
with emphasis
on coordinating
any exceptions
to specific surveillance
activities with managers
and engineering.
Additionally, instructions
were issued to document exceptions
on both the shipping release
forms
and surveillance
reports
along with identifying who concurred with
the exceptions.
Finally, to reinforce the above effort, the manager
of materials
and procurement,
by memorandum
dated
December
21,
1990,
reminded all employees
in this group of the
need to implement these
corrective measures.
(CLOSED)
IFI
259,
260,
296/91-02-03,
Possible
Single
Failure
Criteria Identified with SBGT.
The inspector
documented
the results
of
a test
performed
by the
licensee
in this report.
The test
indicated that with all three
trains of
SBGT initiated and
one of the train fans failed to start
the system will still meet the minimum flow requirements
as stated
in
the
FSAR.
(CLOSED)
URI 259, 260/89-56-02,
Use of Closed
Manual
Valves in
Line Control
Bay Chi llers.
This
item
was identified in. the
course
of observing
check
valve
maintenance
activities.
During an intrusive inspection,
TVA found
that
two check
valves,67-652
and
67-653
had
been
stuck
open.
Following discussions
with the cognizant
TVA system engineer
and
by
reviewing
FSAR Section
10. 10.3
and the applicable flow diagram
no.
1-47E859-1,
the
NRC inspection,
noted
an apparent
discrepancy
between
the
FSAR's
description
of the
system
and its operational
alignment.
In addition,
the
NRC
team questioned
whether the
two
check
valves
were
necessary
by design
conditions
since
they were
installed
in tandem
and
located
immediately
downstream
of manual
isolation valve 67-651 which is normally closed.
In response
to the stated
concerns,
TVA agreed that the
FSAR does not
fully discuss if the
EECW isolation valves which affect the supply of
cooling water to the control
bay chillers
have automatic actuation
and indicated that Amendment
8 to the
FSAR will include
a revised
and
correct description of the
EECW system.
In reference
to the team's
second
concern,
TVA indicated that the
check
valve
configuration
is
correct.
In their
present
configuration,
the
subject
valves
by design
maintain
associated
separation
when the manual
isolation valves
are
opened (i.e.
supplying
EECW to the control
bay chillers).
TVA indicated that
these
valves
prevent
backflow when
one of the associated
experience
a
loss of flow condition.
With regards
to the
code
requirement
that these
valves
be exercised
once every three
months,
TVA requested
and
was
granted relief from this requirement for six
including the
two subject valves.
As an alternate
to
the
Code requirement,
TVA will disassemble
a minimum of two check
valves at each refueling outage
on
a rotational basis,
to verify its
32
backseating
capability.
Should
the
disassembled
valves fail to
function properly, all
other
valves
in this
category will be
disassembled
and examined.
These
valves will be full stroked in the
open position quarterly
as required.
(CLOSED)
URI 259, 260, 296/90-29-04,
Deletion of ECNs/DCNs.
This
item
was that
ECNs/DCNs
were
being
deleted
from the Unit 2
restart list without proper review by the
CCB or middle management.
Eight of the
commitments
were listed
as
NRC
commitments.
The
inspector
reviewed the licensee's
closure
package for this item.
The
licensee's
evaluation
determined
that in none of the
cases
was
an
actual
NRC commitment deleted.
Five were determined
to not involve
NRC commitments,
three
items were rescheduled.
The categorization
as
a
NRC commitment
by the licensee is done
by the
DCN initiator.
This
initial categorization
is superseded
by the
CCB Subcommittee/Restart
Review
Subcommittee.
The
inspector
reviewed
each
of the eight
DCNs/ECNs.
One
example for ECN P0422,
was that the portion of'he
modification affecting Unit
2
was
complete.
The deferral
was for
Units I and
3 modification which continue
to
be tracked
as
NRC
commitments.
Based
on the review of the eight items
the inspector
concluded
there
was
a logical basis for disposition of each
item and
the program
was adequately
implemented.
(CLOSED)
259,
260,
296/90-33-04,
Hardware Activities Delayed
but not Approved by Senior management.
This item was originally identified during reviews of the licensee's
SPOC process.
The inspector
observed
and reviewed various activities
involving system
components
which were
being
delayed
and did not
appear
to have senior
TVA management
approval.
The licensee's
final
determination
as to system operability by TS required that
a system
plus its
attending
components
must
be
to satisfy
TS.
Regardless
of what sequence
is
used
to correct hardware
items, all
must
be completed prior to declaring
a system operable
(CLOSED)
259,
260/90-40-01,
Deficiencies
Identified
During
Integrated
ESF Testing.
This item
was identified
when
the Units 1/2
A and
D did not
accept the
ECCS loads
as required
by the applicable SI.
The licensee
traced
the
problem to
a cell switch that did not make
up properly.
This switch failure was determined
to be an adjustment
problem.
The
licensee
installed
a modification in the Units I/2
as
discussed
in the closure of LER 259/91-01,
in this report.
The licensee
did
not install
the modification in the Unit 3
DGs.
Consequently
296/90-40-01 will remain
open
pending restart of Unit 3.
(CLOSED)
260/90-40-06,
Reliability
and
Human
Factors
Concerns.
33
This
item
was
opened
to follow-up on the licensee's
actions
to
resolve
issues
identified by the
NRR staff audit of the
BFN Unit 2
conducted
in November,
1990.
These
issues
are
addressed
in
detail
and closed
in this report.
This
open
item also included
two additional control
room indication
issues
identified in
IR 90-40.
During this reporting period,
an
inspector
reviewed
the
licensee
actions
taken
to close
the
two
issues.
The issues
and actions
taken were
as follows:
1)
Issue:
Suppression
chamber
water
level
instruments
2-
LI-64-54A and 2-LI-64-66, with
a
range of negative
25 to
positive
25 inches,
lacked indications of negative values.
Action:
The scales for these
instruments
were changed
out with
appropriate
scales
showing positive and negative values.
2)
Issue:
B
channel
recorder
XR-64-159,
Suppression
Chamber
Water Level
and Drywell Pressure,
had
no units designation
label.
Action:
Unit designation
labels for feet
and psig were
added
as operator aid number 2-91-11.
No deficiencies
were identified during the inspector's
review.
The
inspector
concluded
that
no violation of
NRC requirements
had
occurred
and the licensee
had resolved
the issues
involved.
(CLOSED)
260/90-18-04,
Failure
to
Control
Modifications
Activities.
On
May 29,
1990,
a Dresser
Coupling failed
on an
18 inch diameter
section of piping in the 3B/3D
RHRSW Tunnel.
The failed coupling was
on the
North Supply
Header prior to the Unit 3 Reactor
Building
The failure occurred
during modification work on
a
support
and
was
the direct result of failure
by
modifications
personnel
to
obtain
permission
from
the
Shift
Operations
Supervisor to work on this section of piping while it was
in service.
SDSP-7.9,
Integrated
Schedule
and
Work Control, Section
6.4.1,
required that prior to commencing
work activities that
have
the
potential
for affecting
equipment
operation,
that
a
Plant
Operation
Impact Evaluation
Sheet
be filled out.
In this case
the
Plant Operation
Impact Evaluation Sheet
had
been
approved for work on
the
south
only.
Upon removing bolting from the nearby
support
the piping separated
at the coupling.
When the coupling
failed large
amounts of water discharged
into the piping tunnel with
personnel
in the tunnel.
The inspector
reviewed the licensee's
response
to the violation dated
August
13,
1990.
In that
response
the
licensee
attributed
the
violation to personnel
error, i.e. failure of modification personnel
to recognize
that authorization
to implement the workplan
had
been
denied.
As corrective action the licensee
took disciplinary action
against
the craft
foreman.
Additionally, based
on
reviews of
calculations
of piping and support stress
levels experienced
during
the event,
TYA determined
that support
loads did not exceed
design
allowables.
Pipe stresses
were within code allowables
except for a
weldlet attachment
of
a three
inch diameter
pipe to the
18 inch
The inspector
reviewed Final
Event Report I-I-B-90-061 which provided
the licensee's
investigation of the event.
The inspector
noted that
the licensee
had adequately
determined
the root cause of the failure
and
took appropriate
corrective
action
as
the result
of this
investigation.
The damaged
three inch weldlet was replaced
under
DCN
W7630B
as
implemented
under
WP 0458-90 which was completed
on August
25,
1990.
Additionally, during the original inspection the inspector identified
concerns
about the operability of the retention pins
and the adequacy
of the sequencing
criteria for axial
support
removal.
During the
licensee's
evaluation
of the
event it was
determined
that
the
retention
pins
had
been
operable prior to the event
and
had
been
sheared
when the coupling failed.
Since
the pins in question
are
intended
to maintain
the coupling position
on the pipe and are not
designed
to hold the piping together
under the thrust loads
as were
generated
from this event
the inspector
agrees
with the licensee's
determination.
The licensee
revised
the sequencing
instructions
on
Drawing 47B435-22 to clarify requirements
for modification sequencing
of axial support
removal.
This adequately
addresses
the inspectors
two concern.
Based
on the above review the inspector
determined that the licensee
had
performed
adequate
corrective
actions
which should
prevent
recurrence.
(CLOSED)
VIO 259,
260,
296/90-29-01,
Failure
to Control
Work
Activities.
During
a review of licensee
controls for work activities
on plant
equipment
the
inspector
identified
two examples
of failures
to
adequately
control
work within the
requirements
specified
in the
existing clearance
program.
Subsequent
to issuance
of this violation
the
inspector
identified
two
new events
which were
included
as
additional
examples
to this violation.
These
new examples
were
discussed
in IR 90-33.
The
inspector
reviewed
the licensee's
responses
to the violation
dated
December
28,
1990,
and January
31,
1991.
In those
responses
the licensee attributed the violation to personnel
errors rather than
the result of programmatic
deficiencies
in the hold order process.
This determination
was confirmed by an independent
review conducted
by the onsite
gA organization.
As corrective action the licensee
I
~
~
~
35
committed
to conduct sensitivity training of associated
personnel
(system
engineers,
operations,
maintenance,
and
modifications
personnel)
and
strengthen
the training
program for personnel
that
routinely hold clearances.
Additionally the licensee
committed to
completion of
a
HPES evaluation
of these
events.
Any corrective
actions identified by this evaluation
would also
be completed.
The inspector
agreed
with the
licensee's
determination
that
the
failures
were
not
due to programmatic
deficiencies,
i.e. that the
hold order
process
was basically
sound
and that the failures
were
failures to properly implement existing requirements.
The inspector
reviewed
records
to verify the completion of the required training.
Additionally the inspector
reviewed
the
completed
HPES evaluations
and associated
recommendations.
The inspector
determined
that the
completed
corrective
actions
should
be
adequate
to
preclude
recurrence.
n.
(CLOSED)
VIO 259,
260,
296/90-33-01,
Failure to Nake
and 50.73 Reports.
This VIO was issued for two examples of the failure to notify the
NRC
of unplanned
ESF actuations
and
one example of the failure to submit
a
LER on
a condition prohibited
by TS.
Example
A involved the
failure to notify the
NRC within
4
hours
of
an
unplanned
isolation of the
RWCU system
which occurred
on October
20,
1990.
Example
B involved the failure to notify the
NRC within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> of an
unplanned
ESF isolation of the Refuel
Zone ventilation system
which
occurred
on
November
4,
1990.
Example
C involved the failure to
submit
a
LER to the
NRC within 30 days for the failure to maintain
a
TS required fire watch.
The licensee
responded
to this YIO by letter on January
16,
1991.
In
the response,
the licensee
denied
example
8 because
the isolation was
given
from
a pressure
instrument
which
was
not part of the
initiation signal.
After review of the circumstances,
the
NRC staff
accepted
the licensee's
denial of example
B by letter on February 28,
1991.
The staff also concluded that the responses
to examples
A and
C were acceptable.
An inspector
reviewed the licensee's
response
and closure
package for
this VIO.
Following issuance
of the violation, the licensee
made the
required
10 CFR 50.72 notification for example
A of the violation and
issued
LERs for
examples
A
and
C
(296/90-04
and
259/90-21,
respectively).
was
closed
in
IR 90-40
and
was
closed
in
IR 91-06.
No further
concerns
were
identified during the review of the licensee's
actions.
t
14.
Condition Adverse to gquality Reports
The inspector
reviewed
3 CARR's concerning welding activities to determine
if any hardware
problems existed in the plant.
36
a.
CARR 900317, Failure to Perform Fitup Verification, Unit 2
This item pertains
to inspection
and control of welding activities
associated
with modification of Unit
2 drywell
Non-ASME structural
steel.
The item was identified during the conduct of a
gA audit of
welding activities
in September
1990.
At that
time
a
concerned
individual informed the
TVA auditors that
some iron worker foreman,
were not entering
the drywell area to physically inspect weld fit-up.
The findings of
a followup investigation
disclosed,
that
between
December
11,
1989,
and January
19,
1990,
a modification foreman
had
signed fitups verification for twenty safety related structural
steel
welds all located
inside the drywell,
on dates
when entry records
~ showed that
he
had not entered
the Unit 2 drywell.
Procedure
SDSP
13.8, Welding Surveillance,
Section 6. 1, directs the craft foreman to
perform weld fit-up inspections
for instances
where certain
specifications
and
other
nuclear
construction
standards
were
referenced
by design output documents.
A fit-up Inspection
includes
verification of:
Weld joint dimensions (fit-up)
Proper material
Welder qualification
Proper welding procedure
Surface cleanliness
Alignment
Preheat
temperature
Tack welds
Following discussions
with cognizant
personnel
and
a comprehensive
records
review the inspector ascertained
the following:
Because
the
concern
originally implicated three
iron worker
foremen,
TVA modification
management
determined
that
a full
investigation
of all
iron worker
foremen
was
necessary
to
determine
the generic
aspects
of the issue.
The method
TVA used
to
pursue
this
task
included;
( 1) identification of all
work-plans inside
the drywell implemented
by iron workers;
(2)
development of an accurate list of iron worker foremen
who were
actively involved in these work-plans;
(3) for every individual
identified on the list, radiation control
was asked to generate
a printout
showing all entries
to the
drywell
dur ing the
time-frame of interest.
made
in the modifications'ab
shops
and welders
who fabricated
them were excluded
from the
investigation.
Corporate
NDE personnel
provided
assistance
in the investigation.
The records
showed that out of the
20 field welds in question,
four
had
been
selected
for inspection
of fit-up by
gC
as part of the
random
inspection
program for these class/type
welds..
In addition,
the records
show that following welding, all
20 of the subject welds
received
and
passed
a final visual inspection that
was
performed
by
I'
37
gC under
programmatic
requirements
and applicable
procedures.
To
demonstrate
that
even
though
the
iron worker
foreman failed to
perform the administrative
task of conducting
a fit-up inspection
prior to welding
TVA took the position that all of the attributes
associated
with this inspection
were verified at
some
time during
fabricating
of
these
In
support
of this
position,
documentation
in the
CARR package
stated
the following:
For each of the subject
20 welds, three of the preweld fit-up
activities/attributes
referenced
above,
were
checked
and
documented
by a foreman
on
a weld data
card.
These activities
were
performed
as
the
foreman
assigned
(a) certified welders
with current qualifications,
(b) proper detail
weld procedure
and (c) proper filler metal.
These
three activities
were also
verified
as
acceptable
during final visual
examination
by
quality control.
Three additional
preweld activities/attributes
which required
foreman
verification were:
proper material
alignment
weld 'joint dimensions (fit-up including root gap)
These
activities
were
performed
by
the
designated
welder
and
documented
on the appropriate
form.
One of the attributes
that
could
not
be verified during final
inspection
by quality control
was
preheat.
Having the correct
preheat,
as required
by the applicable
weld procedure,
is incumbent
upon
the designated
qualified welder.
The foreman administratively
checks
that
the correct
preheat
was
achieved
prior to welding.
However,
by specification
and
on the basis of material
size
and type,
none of the structural
steel
welds under discussion
required preheat.
Therefore,
the failure by the foreman to check the preheat prior to
welding would have
no impact
on the integrity of the subject welds.
Another of the attributes that could not be verified visually during
final inspection
by gC was the fit-up gap.
This is another of the
attributes
whose verification is incumbent
on the designated
welder
as
part of his responsibility
for good workmanship of his welds.
Also, it is
one of the attributes
that the
foreman
must
check to
assure
that
the correct
gap
was
achieved
prior to welding.
By
procedure,
the welder
measures
and
documents
on the weld history
record the root gap dimension.
This was
done for each of the subject
knowing the correct
gaps size allows
gC to verify correct weld
size,
since
the leg of
a fillet weld is dependent
on the root gap
size.
As stated
ear lier,
the
in question
were usually
inspected
and
found acceptable
therefore, it would appear
that the
fai lure of the iron workers'oreman
to perform the required
fit-up inspection
would not have
an adverse
impact on weld integrity.
r
~
I
0,
38
In the broader
scope of this investigation,
gC performed
a review of
records
generated
by the modification of drywell structural
steel.
The
review of the
records
showed
that
these
had
received
a final visual
examination
by gC and were found acceptable.
The records
also
showed that,
as part of the
on going structural
steel
welding program,
gC performed preweld checks
on
a random sample
of
1265
selected
from
a total
population
of 3328
fabricated
from November
1989 to April 1990 regardless
of welder
foremen.
Out of this
sample,
approximately
38Ã of the total
population,
TYA's review identified
39 unacceptable
hardware
and
software
conditions
for
a
3Ã rejection
rate.
The
unacceptable
conditions identified have
been corrected.
To explore
the
generic
aspects
of this matter,
records
of
gC
inspections
performed
between
August
1989
and
August
1990
were
reviewed
by TVA with emphasis
placed
on all the foremen
who worked
on
modifications of structural
steel
welds inside Unit 2 drywell.
The
records
review included
inspection
performed
on structural
steel
welds in other areas
of the plant where
foremen
under investigation
were involved.
Out of
a total population of 3236 welds,
792 weld
records
were
reviewed
by
gC
who discovered
that
none of the welds
were
found unsatisfactory.
. The
records
showed
that
26
exhibited conditions which COTS.
Fifteen of the
COTS items pertained
to hardware
and
included
stamping
the material incorrectly, fitups
that were in disagreement
with design
drawing requirements,
and paint
in the weld area.
Eleven
software
problems identified,
included
failure to document
and correct errors without initialing and dating
the correction.
No rejects
or
COTS items
were written regarding
preheat or fitup gap discrepancies.
In conclusion,
the inspector
considers
the licensee's
present
welder
training program
a weakness
and
an area requiring improvement.
For
example,
records
show that iron workers
are
given approximately
45 minutes to one hour training on procedures
and specifications i.e.
SDSP-13. 1, 13.4,
13.8,
G-29.
The inspector
was given to understand
that
the training
sessions
are
informal
and
lack
the
necessary
programmatic
structure
and/or
testing
for the participants
to
demonstrate
proficiency in the material
presented.
CARR 910080,
Welding/Grinding Performed
on Sacrificial Shield
Wall
Liner Plate Without Appropriate Documentation
or Inspection,
Unit 2.
This item was identified when
a concerned
individual reported that
welding
had
been
performed
on
the liner plate
and
subsequently
removed without appropriate
documentation
having
been
issued prior to
work being
performed.
The inspector
discussed
this matter with
cognizant licensee
personnel
and reviewed the data
package
presented.
Through this effort, the inspector ascertained
that the undocumented
and its subsequent
shield wall liner plate
was located at the
255 Azimuth of the drywell near the
601 ft. elevation.
The welding
and subsequent
grinding occurred
near
a stiffener plate appearing
in
~ (
39
drawing 48W981-2 Rev.3,
System
303
and
shown
as field change
request
FCR
87-1274
on
the
subject
drawing.
Following the disclosure,
WR 303-WO-9127620
was
issued
to remove
the paint from the
area
in
question,
perform
an
acid
etch
and
inspect
the
area.
Upon
completion,
the records
indicated that the acid test confirmed that
welding
had occurred
on either side of the aforementioned
plate.
The area
where welding occurred
was approximately I/2 to 7/8
inches
in width and the affected material
depth
was measured
at less
than
1/32 inches
deep.
The visual examination
records
disclosed that
no
damage
had
been
done to the
1/4 inch thick liner plate material
and that
no additional
rework was required.
In reference
to generic
implications, the
CARR investigation indicated that
no review in this
area
was
necessary
since
the activity in question
was
an isolated
case
of failure to follow procedure
by specific site
personnel.
Additional training
had
been
scheduled
for personnel
implicated in
this matter.
Records
showed that this item was not subject to review
by the
restar t committee
and
therefore
closing of the
item
was
recommended.
CARR 910064, Falsification of Welder Continuity Records.
Welder
certification
continui ty is
maintained
by
SDSP
13.4,
Revision 7,
Welding/Brazing/Soldering
Filler Material
Issue
and
Welder/Brazer/Solder
gualification Program.
Paragraph
G.6.2 of the
subject
procedure,
states
in part,
that
welder certification
continuity will be accomplished
upon receiving
one or more
WMR slips,
for each
process
requiring
updating
within the required
90
day
period.
The
WMR slip shall
be signed
by the responsible
foreman,
general
foreman,
or weld test supervisor certifying that the welder
utilized the
process
indicated.
As
a
programmatic
crosscheck,
certification
updates
are
permitted
only upon
the return of used
welding material
stubs
to the issue
center.
The subject
CARR was
written following the disclosure
that two welders
had their process
certification
updated
even
though
they
had
not
used
the welding
process
on the date of certification, nor had they returned
any used
welding material
stubs to the issue station
as required
on the date
indicated.
Details of the
materials,
and
welding
processes
are
as
follows:
Welding Process:
Welding Material:
WP004990-13,
14, 15,
and
16
1-478451-S0276
Shielded
Metal Arc
E7018,
.093
"No Welding Electrodes"
V
0
40
Welders
Implicated
BF704
BF924
Date of Infraction
8/15/90
8/16/90
The above weldments
were not associated
with ASME Code components.
The
licensee's
cause
analysis
report,
dated
February
15,
1991,
disclosed
that
the subject
CAqR was
an additional
example of the
conditions identified by
CARR
BFP 900252
and subsequently
addressed
in Event Report II-B-90-098, Item C, Welding, Brazing,
and Soldering
Material
Control.
The
records
indicated
that
the
subject
CARR
(BFP910064),
was written in the
same
time-frame
and identifies
a
condition similar to the conditions
adverse
to qualities that were
dispositioned
by
CARR BFP90052.
The root causes
identified in the
aforementioned
Event
Report
were related
to personnel,
a lack of
attention
to
details
and
carelessness.
Because
of their
similarities, the root cause of both
CAgRs were found to be the
same.
For corrective actions
based
upon the above mentioned
cause analysis,
TYA's position
was that the
two examples
identified were isolated
instances.
Computer
program driven checks will continue to monitor
and
detect
conditions
such
as
those
identified by the
CARR and
therefore,
no recurrence
corrective action is
deemed
necessary
for
welder certification updates.
In summary,
no
hardware
problems
were identified during the review of
these
CAgRs that would preclude plant restart.
15.
Allegations
RII-90-0081
The concern
was referred
to the licensee
by the
NRC for investigation.
The
inspector
reviewed
the
licensee's
Employee
Concern
Program
investigation
(ECP-90-BF-J25-Fl) of this issue.
The first part of the concern stated that SDSP-7.6.2
was interpreted
to
mean that if a piece of equipment
was taken out of service,
then approved
work instructions
were not necessary
since the equipment did not effect
safety if out of service.
An unapproved
handwritten
instruction
was
sufficient.
Thus,
the instruction would not be approved
or get
a 50.59
review.
The licensee
concluded for part
1 that site procedures
would not
allow work to
be
accomplished
with unapproved
work instructions.
The
inspector
reviewed
SDSP 7.6, Maintenance
Management
System,
Revision
11,
and validated the licensee's
determination that work must
be accomplished
using
an approved
work order.
SDSP 7.6.2,
Planning
Work Orders,
contained
the administrative controls for the planning process,
including generation
of work orders.
The inspector
noted that the requirements
for equipment
in-service
and
out-of-service
in
SDSP
7.6.2 differed
only in that
equipment
in-service that
must
be manipulated
required manipulation
by
approved instructions
rather
than
as part of an approved
work order.
The
inspector
discussed
the interpretation
of these
sections
with several
licensee
employees
who are in the planning group.
All agreed that any
41
work accomplished
must
have proper approvals.
The inspector
reviewed
gA
monitoring reports for 1990
and
1991 associated
with work orders
and noted
that
5 reports
identified
work orders
that
had
been
revised
without
obtaining the proper approvals.
None of the revisions
required safety
assessments.
The
purpose
of SDSP 7.6.2
was to ensure
that all maintenance
activities
under the work order process
return equipment, structures,
and components
to their design specifications.
The inspector
reviewed
SDSP 27. 1, Safety
Assessment/Evaluation
of Changes,
Tests,
and
Experiments
which implements
the licensee's
10 CFR 50.59 program.
The inspector
noted
in the definitions section
under
"Changes
in the Facility as Described
in
the Safety Analysis Report", that maintenance
activities
which did not
result in
a change
to the system or which replace
parts with like parts
did not require
a safety
assessment
or safety
evaluation.
Since
maintenance
work orders
were required to be approved
and return equipment
to their original
design configuration,
which
was not
a
change
to the
facility, the inspector
was unable to substantiate
the first part of the
concern.
The
second
part of the concern
stated
that Standard
10.3.2
was
approved
without a 50.59 review, but implemented
SDSP-6.7
which did require
a 50.59
review.
This
was
also
a
problem at
Sequoyah.
Both the licensee's
investigation
and the inspector
found the second part of the concern true,
but not
a problem.
All corporate
standards
must
have site
implementing
procedures,
which get 50.59 reviews.
Therefore,
the corporate
standard
gets
a 50.59 review when
implemented at each site.
The third part of the concern stated that SDSP-6.7,
page
10,
and
Form 292
do not require
a 50.59 review for creating
a Post Maintenance
Test.
This
is
a conflict with SDSP-2.11.
The licensee's
investigation concluded that
post maintenance
test instructions
documented
on Form 292 got
a qualified
review
by
an engineer,
who determined
whether
a safety
assessment
was
needed.
The inspector
noted that SDSP-6.7,
revision 4, effective December
6,
1989
(an earlier revision),
did not contain
any reference
to 50.59
reviews.
The inspector
reviewed the portion of SDSP-6.7,
Post Maintenance
Test Program,
revision
7 (current revision), which contained instructions
for filling out
Form 292.
The inspector
noted that paragraph
6.3.2.1
tells
the
reviewer
to
perform
a
safety
assessment
as
required
by
SDSP-27. 1.
The inspector
reviewed
SDSP 27. 1, revision
12 but did not find
any guidance
to determine
when
a post maintenance
test would or wouldn'
require
a safety
assessment.
Since the reviewer
was not required to have
had
any 50.59 training (Level I or II), the inspector
was concerned
that
SDSP-6.7
and
SDSP-27. 1 left the reviewer without any guidance
to decide
whether the
Form 292 needed
a safety assessment.
The inspector
considered
how other test instructions
are
reviewed
on the
site.
SDSP-2. 11
was
replaced
by
SSP-2.3,
Administration of Site
Procedures.
SSP-2.3,
Revision 1, Section 3.3, states
that procedures
that
are quality related
or are
required
by Technical
Specifications
are
required
to
have
a safety
assessment
performed prior to approval.
The
t~"
P
0,
42
licensee
indicated that most post maintenance
tests
were performed using
a
portion of
a surveillance
or testing instruction.
Therefore,
the post
maintenance
test
would
have
already
had
a safety
assessment.
The
inspector substantiated
the concern that SSP-2.3
and SDSP-6.7 conflict in
relation to the fact that not all post maintenance
tests
may get
a 50.59
review.
However,
some
may not require reviews if adequate
justification
were provided in SDSP-6.7.
The licensee initiated
a change
to
6.50
that will require
a safety
assessment
anytime
a
Form 292 or equivalent is
used.
The failure of SDSP-6.7
to provide adequate
guidance
on
when
a
safety
assessment
is
needed
for
a
FORM
292
post
maintenance
test is
considered
a violation of
TS 6.8. 1
and is designated
NCV 259,
260,
296/91-10-04.
This
NRC identified violation is not being cited
because
criteria specified
in Section
V.A of the
NRC Enforcement
Policy were
satisfied.
The inspector
noted several
weaknesses
in the licensee's
investigation
in that it did not look at the implementation of the work
order
process
nor at whether criteria existed
to determine
whether
a
safety assessment
was
needed for Form 292.
Information Meeting With Local Officials (94600)
On
March
22,
1991,
a meeting
was
held with the
Athens City Mayor,
Limestone
County
Commission
Chairman,
and
Athens-Limestone
Emergency
Management
Agency Director
and the
NRC TVA Projects
Branch Chief, Section
Chief, and Senior Resident
Inspector.
The plans for the restart of Unit 2
were discussed.
Several
other
items were discussed
including historical
problems at the plant, siren testing,
and involvement of TVA in community
activities.
The meeting
was beneficial
and informative.
The local public document
room at the Athens Public Library was inspected
on March 22,
1991.
NRC documents
were readily available for review by the
public.
Exit Interview (30703)
The inspection
scope
and findings were
summarized
on April 25,
1991 with
those
persons
indicated
in paragraph
1 above.
The inspectors
described
the areas
inspected
and discussed
in detail the inspection findings listed
below.
The licensee
did not identify as proprietary
any of the material
provided
to or
reviewed
by the
inspectors
during this
inspection.
Dissenting
comments
were not received
from the licensee.
Item Number
2590
260, 296/91-10-01
259, 260, 296/91-10-02
Description
and Reference
URI, TS Requirements
During Check Valve
Testing,
paragraph
3.
VIO, Missed Compensatory
Samples,
paragraph
3.
259, 260, 296/91-10-03
VIO, Inadequate
Test Control, paragraphs
4
and 12.
43
259, 260, 296/91-10-04
NCV, Safety Assessment
for PMT, paragraph
15.
Licensee
management
was
informed that
5 TMI Action Items,
6 LERs,
6 IFIs,
5 URIs, and
3 VIOs were closed.
and
AOI
ATU
BFNP
CAQR
CCB
CCD
CFR
COTS
DBVP
DCN
DGVA
GL
HED
HPES
Initial isms
Alternating Current
Automatic Depressurization
System
Abnormal Operating Instruction
Analog Trip Units
Browns Ferry Nuclear Plant
Boiling Water Reactor
Owners
Group
Boiling Water Reactor
Containment Air Dilution
Continuous
Atmosphere Monitors
Condition Adverse to Quality Report
Change Control
Board
Configuration Control Drawing
Cubic Feet
Per Minute
Code of Federal
Regulations
Corrected
On The Spot
Control
Rod Drive
Chemistry Shift Supervisor
Design Baseline Verification Program
Drywell Control Air
Direct Current
Design
Change Notice
Diesel
Generator
Diesel
Generator
Voltage Available
Engineering
Assurance
Emergency
Core Cooling Systems
Engineering
Change Notice
Employee
Concerns
Program
Emergency
Equipment Cooling Water
Electrical Maintenance
Instruction
Emergency Notification System
Emergency Operating Instruction
Emergency
Procedure
Guidelines
Engineered
Safety Feature
Fuel
Load Chamber
Final Safety Analysis Report
Flow Control Valve
General
Electric
Generic Letter
Human Engineering
Discrepancies
High Pressure
Coolant Injection
Human Performance
Enhancement
System
44
IFI
IIR
IR
ISPDS
KW
LCO
LER
LRED
MMI
NI
NQASE
NRC
NVA
PEG
PMI
Psig
RCW
RMOV
SDSP
SMPL
Heating, Ventilation,
8 Air Conditioning
Inspector
Followup Item
Incident Investigation Report
Integrated
Leak Rate Test
Intermediate
Range Monitor
Inspection
Report
Interim Safety Parameter
Display System
Kilowatt
Limiting Condition for Operation
Licensee
Event Report
Local
Power
Range Monitor
Licensee
Reportable
Event Determination
Mechanical
Maintenance
Instruction
Maintenance
Request
Non-Cited Violation
Nondestructive
Examination
Nuclear Instrumentation
Nuclear Performance
Plan
Nuclear Quality Assurance
and Engineering
Nuclear Regulatory
Commission
Normal Voltage Available
Primary Containment Isolation System
Project Engineering Guidelines
Plant Manager Instruction
Preventive
Maintenance
Post Modification Test Procedure
Post Modification Testing
Pressure
Suppression
Chamber
Pounds
Per Square
Inch
Pounds
Per Square
Inch Gauge
Quality Assurance
Quality Control
Reactor
Core Isolation Cooling
Raw Cooling Water
Residual
Heat Removal
Residual
Heat Removal Service
Water
Radiochemical
Laboratory Analyst
Radiation Monitor
Reactor Motor Operated
Valve
Reactor Operator
Reactor Protection
System
Reactor
Pressure
Vessel
Standby
Gas Treatment
Site Directors Standard
Practice
Surveillance Instructions
Site Master Punchlist
45
SOI
SPAE
SRN
TD
TI
TS
WMR
WP
Speci al Operating
Ins true tion
System Plant Acceptance
Evaluation
Safety Parameter
Display System
System Pre-Operability Checklist
Source
Range Monitor
Senior Reactor Operator
Site Standard
Practice
Test Deficiency
Technical Instruction
Three Nile Island
Technical Specifications
Valley Authority
Violation
Vertical Slice Review
Welding Material Requisition
Work Order
Work Plan
Work Request
1h
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