ML17251A152
| ML17251A152 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 06/24/1988 |
| From: | Snow B ROCHESTER GAS & ELECTRIC CORP. |
| To: | Russell W NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| References | |
| NUDOCS 8807070389 | |
| Download: ML17251A152 (12) | |
Text
ACCELEMTED DISFRIBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8807070389 DOC.DATE: 88/06/24 NOTARIZED: NO DOCKET FACIL:50-244 Robert Emmet Ginna Nuclear Plant, Unit 1, Rochester G
05000244 AUTH.NAME AUTHOR AFFILIATION SNOW,B.A.
Rochester Gas
& Electric Corp.
RECIP.NAME RECIPIENT AFFILIATION RUSSELL,W.T.
Region 1, Ofc of the Director
SUBJECT:
Responds to violations noted in Insp Rept 50-244/88-08.
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TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation sponse NOTES:License Exp date in accordance with 10CFR2,2.109(9/19/72).
05000244 RECIPIENT ID CODE/NAME PD1-3 PD INTERNAL: AEOD NRR MORISSEAU,D NRR/DLPQ/QAB 10 NRR/DREP/EPB 10 NRR/DRIS DIR 9A NUDOCS-ABSTRACT OGC 15-B-18 RES/DRPS DEPY RNAL: LPDR NSIC COPIES LTTR ENCL 1
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RECIPIENT ID CODE/NAME STAHLE,C, DEDRO NRR/DLPQ/PEB 11 NRR/DOEA DIR 11 NRR/DREP/RPB 10 NRR/PMAS/ILRB12 OE LIE ERMAN,J REG FILE 02
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ROCHESTER GAS AND ELECTRIC CORPORATION o 89 EAST AVENUE, ROCHESTER, N.Y. 14649.0001 TCLCP~O" C A+CA COOK Zlc 546 2700 June 24, 1988 Mr. William T. Russell Regional Administrator U.S. Nuclear Regulatory Commission Region I 475 Allendale Road King of Prussia, PA 19406 Inspection Report 50-244/88-08 Notice of Violation Ginna Nuclear Power Plant t No. 50-244
Subject:
R.E.
Docke
Dear Mr. Russell:
Inspection Report 50-244/88-08 Appendix A, stated in part:
lA.
Technical Specification 6.8.1 requires written procedures shall be established, implemented, and maintained covering activities referenced in Appendix A of Regulatory Guide 1.33, November 1972.
Appendix A addresses procedures for General Plant Operations (paragraph B),
and Equipment Control (paragraph A).
Licensee operations procedure 0-1.1, Plant Heatup From Cold Shutdown to Hot Shutdown,
- requires, in part, valve 879 (safety injection test line outside containment isolation valve) be locked closed.
During the inspection conducted on April 6 - May 8,
- 1988, and in accordance with the General'tatement of Policy and Procedure for NRC Enforcement Actions 10 CFR Part 2, Appendix C (Enforce-ment Policy 1986), the following violation was identified:
+go I SS070703S9 SS0624 PDR ADOCK 05000244 PDC
Contrary to the
- above, on April 5,
- 1988, with the plant operating at approximately 100 percent power, the licensee discovered valve 879 unlocked and open.
1B.
Licensee Administrative Procedure A-1401, Station Holding
- Rules, requires:
"The securing and restoration of all apparatus affected by the "hold" shall be effected by an operator and verified by a second operator or STA."
Contrary to the
- above, on April 17,
- 1988, the resident inspector identified that during the securing and restora-tion of a portion of the Boric Acid System for repair two valves repositioned as part of the "hold" were not effec-tively tracked and/or verified and consequently were not repositioned properly following the "hold" restoration.
VIOLATION lA Rochester Gas and Electric Corporation (RG&E) agrees with Violation lA as stated.
This event was initially identified on April 5, 1988 by RG&E during the performance of PT-2.1 (Safety Injection System Pumps).
Test personnel, while performing the initial lineup for PT-2.1, found Valve 879 in the open position.
Controlled by A-52.2 (Control of Locked Valve and Breaker Operation),
valve 879 is a
locked closed valve.
The following is RG&E's explanation and reply to this statement
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of violation 1A:
Reason for the violation:
2
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RG&E investigations revealed that the last documented stroking of Valve 879 was March 24, 1988 during plant heatup.
Procedure O-l.l step 5.55.10 directs valve 879 be locked closed.
This step was not performed completely and no independent verification documentation of the valves position was performed.
Corrective Steps Which Have Been Taken and the Results Achieved:
Valve 879 was closed and locked and a
complete Safety Injection System lineup outside containment was performed.
The results of the lineup check were that the Safety Injection System, with the exception of valve 879 had been correctly aligned for power operation.
Also the following valves were verified closed which provided isolation even with valve 879 open:
Valves 879A, 879B 879Cg 884'nd 2818 (reference RG&E Drawing 33013-1262). It was determined that with valve 879 open and the above valves closed the operability of the Safety Injection System was unaffected.
An interim policy on double verification was issued by the Operations Manager requiring the following in regard to realignment and verification of safeguards or Technical Speci fication related systems following maintenance, modifications, testing or other operational activities:
a ~
b.
All isolations and realignment shall be done in accordance with a
procedure or a 'system/equipment alignment worksheet which requires two independent signoffs for each realignment.
All realignment steps in existing procedures shall be signed off by two persons knowledgeable in the system operation, the first being the actual realignment and the second being an independent verification.
3 ~
Corrective Steps Which Will Be Taken To Avoid Further Violations:
4
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An administrative procedure is currently being developed that will provide the specific guidance on accomplishment of independent verification, including the interim policy.
This procedure will be in effect by September 2,
1988.
Date When Full Compliance Will Be Achieved:
Full compliance with the proper alignment was achieved on April 5, 1988 with the closure and locking of valve 879.
VIOLATION 1B RG&E agrees with the violation as stated.
This event was initially identified on April 17,
- 1988, by the NRC resident inspector.
During a weekend plant tour, the inspector identified valves 332 and
- 340, in the Boric. Acid System, open.
Procedure S-3.1B (Pre-operational Lineup Of Boric Acid System) and Station Flow Print 33013-1266 (Boric Acid), require both valves closed.
The following is RG&E's explanation and reply to this statement of violation 1B:
Reason for the violation:
2 ~
RG&E investigations revealed that the valves were reposi-tioned when part of the Boric Acid System was isolated and held to repair a small leak.
Although valves 332 and 340 were repositioned they were not tracked as part of the
<<hold".
When the Boric Acid System was restored following removal from "hold"
- status, valves 332 and 340 were overlooked.
Both valves remained open with the filter unisolated and therefore did not affect the operability of the Boric Acid System (referenced RG&E Drawing 33013-1266).
Corrective Steps Which Have Been Taken and the Results Achieved:
i 4 ~
The resident inspector notified RG&E who verified the valves
- open, closed them and checked the Boric Acid System alignment by performing procedure S-3.1B.
The results of the lineup check were that the Boric Acid Syst: em with the exception of valves 332 and 340 had been correctly aligned for power operation.
Also see Item= 2 violat'ion 1A (Interim Policy On Double Verification).
Corrective Steps Which Will Be Taken To Avoid Further Violations:
An administrative procedure is currently being developed that will provide the specific guidance on accomplishment of independent verification, including the interim policy.
This procedure will be in effect by September 2,
1988.
Date When Full Compliance Will Be Achieved:
Full compliance with the proper alignment was achieved on April 17, 1988 with the closure of valves 332 and 340.
RESPONSE
TO NRC CONCERNS THAT A COMMITMENT MADE BY RG&E IN 1980 TO MEET THE RE UIREMENTS OF NUREG 0737 ITEM I.C.6 WAS NOT MET:
Review of both of the above events by Operation Management and a
previous assessment by
- 0737, Item I.C.6 commitment was.
addressed in various specif ic realignment procedures, there was no administrative guidance which defines the overall methods that are necessary to assure that independent verifications are accomplished.
As a result, an administrative procedure is currently being developed that willprovide the specific guidance on accomplishment of independent verification, including incorporation of the interim policy.
This procedure will be in effect by September 2,
1988.
Very truly yours, Bruce A. Snow Superintendent Nuclear Production BAS/eeh xc:
U.S. Nuclear Regulatory Commission (Original)
Document Control Desk Washington, DC 20555 Ginna USNRC Senior Resident Inspector
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