ML17229A095

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Rev 0 to 00000-OSW-16, In-Situ Pressure Test Results for St Lucie Unit 1 Spring 1996 Outage
ML17229A095
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 10/24/1996
From:
ABB COMBUSTION ENGINEERING NUCLEAR FUEL (FORMERLY
To:
Shared Package
ML17229A091 List:
References
-OSW-16, -OSW-16-R, 00000-OSW-16, 00000-OSW-16-R00, NUDOCS 9610280087
Download: ML17229A095 (24)


Text

St. Lucie Unit I Docket No. 50-335 L-96-273 Enclosure 4 IN-SITUPRESSURE TEST RESUI TS FOR ST. I UCIKUNIT 1 SPRING 1996 OUTAGE REPORT NO. 00000-OSW-16 REV. 00 PREPARED FOR FLORIDAPOWER ANDLIGHTCOMPANY G. C. Fink J. P. Molkenthin J. F. Hall ABBCOMBUSTION ENGINEERING NUCLEAROPERATIONS 2000 DAYHILLROAD WINDSOR, CONNECTICUT 06095 96i0280087 96f024 PDR ADQCK 05000335 P

PDR

1.0 2.0 TABLEOF CONTENTS INTRODUCTION IN-SITU PRESSURE TEST DESCRIPTION

~Pa e

2.1 General 0

3.0 4.0 5.0 6.0 2.2 2.3 2.4 2.5 Localized In-situ Pressure Test Description Summary ofLocalized Tool Uses Summary ofQualification Test ing Test Condition Adjustments ST. LUCIE-1 TEST PROCEDURES RESULTS CONCLUSIONS REFERENCES 14 17 18 ATI'ACHMENTA-Test Report - STEAM GENERATOR TUBE IN-SITUHYDROSTATICPRESSURE TEST TOOL HYDRO CHAMBERPRESSURE DETERMINATION A-1

Title LIST OF TABLES

~Pa e ST. LUCIE-I IN-SITUPRESSURE TEST RESULTS 16

0

LIST OF FIGURES

~Fi ure 2-1 Title Schematic ofIn-situ Pressure Test Tool

~Pa e

10

Section

1.0 INTRODUCTION

This report presents the results of in-situ pressure testing of 17 St. Lucie Unit 1 steam generator (SG) tubes during the Spring 1996 refueling outage.

The tubes that were tested had eddy current test (ECT) indications of various types including upper bundle G.ee span axial indications, axial indications above the tubesheet in the sludge pile, circumferential indications at the top of the tubesheet ( hot and cold leg sides ofthe SG), axial indications at the eggcrate tube supports, and axial, circumferential and volumetric indications at the partial drilled support plates near the top of the tube bundle. The objective ofthe in-situ pressure testing was to demonstrate that tubes which contained large defects, as indicated by ECT examination, nevertheless, fullymet the requirements of USNRC Regulatory Guide 1.121 (Draft), "Bases for Plugging Degraded PWR Steam Generator Tubes" u1.

This objective was accomplished by pressurizing the tubes to the levels required by Reference 1 and observing for indications of leakage and/or structural failure (burst) ofthe tubes.

St.

Lucie-1 is a two loop PWR designed by Combustion Engineering which commenced commercial operation in 1976 and had operated for 14.7 EFPY as ofthe 1996 refueling outage.

Each of the Series 67 steam generators contains 8519 NiCrFe Alloy 600 tubes with a nominal outside diameter of 0.750 inch and a nominal wall thickness of 0.048 inch.

The tubes were explosively expanded into 21.75 inch thick low alloy steel tubesheets which produced an expansion transition in each tube at the top (secondary face) ofthe tubesheet.

The heat transfer tubes are supported by six to ten horizontal supports.

Six of these are full supports; the others are partial supports that support less than the fuH number oftubes because of the bundle geometry.

The lower eight supports are eggcrate supports formed by interlocking 1

inch and 2 inch wide by 0.090 inch thick carbon steel strips.

The two uppermost supports are solid drilled plates of one inch thick carbon steel.

In addition, the tubes are supported by two diagonal support straps and three vertical supports, also fabricated from carbon steel strips.

Section 2.0 IN-SITUPRESSURE TEST DESCRIPTION 2.1 General The degradation of steam generator tubes leads to a decrease in their load bearing capacity and creates concern about the leak tightness of the reactor coolant system.

When observed, tube degradation results in evaluations to demonstrate that the required structural margins are preserved and that leak rates (should leakage occur) will remain within allowable limits.

Reference l provides the current regulatory requirements for steam generator tubes.

These evaluations may be based on one or more ofthe following:

NDE results (primarily eddy current testing but also ultrasonic test results) combined with analyticaVsemi-empirical calculations ofburst pressures and leak rates.

Laboratory burst and leak rate tests on degraded tubes removed fiom operatmg steam generators.

In-situ pressure testing ofsections oftubes with ECT indications ofdegradation.

Historically, a combination of the first two methods has formed the basis for the required evaluations.

Testing of removed tubes provides the most informative information in that burst pressure that can be correlated with the actual amount of degradation as determined by destructive metallographic examination after burst testing.

However, removal of defective tubes 6'om a steam generator has some disadvantages including radiation dose associated with removal and laboratory activities, cost including possible critical path time, evaluation without the effects of steam generator internals (tubesheet,

supports, etc.), and damage to the tubes during the removal process which can lead to inaccurate burst or leak rate test results or in some cases

inabilityto conduct such tests because ofstructural failure during removal.

The latter is especially true for circumferentially oriented cracks or areas ofintergranular attack.

The use ofNDE results combined with analyticaVsemi empirical analysis provides an economic approach to degradation evaluation, but uncertainties in defect sizing have on occasion resulted in overly conservative assessments ofthe severity ofdegradation.

In an effort to combat these inadequacies, ABB CENO developed an in-situ pressure test technique which has been used for structural integrity/leak-rate evaluations.

Both a full tube technique and a localized test (only a small part of the tube is pressurized) have been used successfully to verify Reference 1 margins were maintained when uncertainties in defect sizing and material properties and the limiting assumptions involved with strength evaluations based on inspection data did not permit the same conclusions.

The use ofthis technique is now suf6ciently widespread that industry guidelines (Reference 2) have been developed to standardize performance of in-situ pressure testing and application of test results.

The Reference 2

procedures and requirements were used to develop the procedure for the St. Lucie-1 testing described in this report.

2.2 Localized In-situ Pressure Test Description The ABB CENO localized in-situ pressure test system consists ofan in-situ pressure test tool for testing localized areas of degraded tubes and the ancillary equipment necessary to pressurize and monitor the tube pressure or leak rate during test.

Figure 2-1 shows the tool used for St. Lucie-1 testing described in this report. The major parts ofthe tool are:

a) a stainless steel upper and lower shaft which have been drilled to permit pressurizing ofthe hydro-test chamber and the gripper and seal bladders.

The two sections ofthe shaft are connected by a spring arrangement which permit the two sections to move independently ofone another and insure axial stresses during the test are comparable to those during a capped tube hydro-test.

b) an upper and lower gripper bladder which, when energized, secures the tool against the ID ofthe tube.

c) an upper and lower seal bladder that seals the hydro-test chamber.

d) various o-rings, sleeves, caps, connectors, etc., required to complete assembly ofthe tool.

In addition to the tool itself, the system consists of a 2 HP air operated Haskel positive displacement pump to provide pressurized water to the test chamber, a smaller air operated Haskel positive displacement pump for energizing the bladder system (both gripper and sealing bladders),

hoses and fittings to connect the tool to the pumps, gauges for monitoring test and bladder system pressures, and a strip chart recorder to document the output of a pressure transducer providing a record of pressure as a function of time.

The strip chart output is the permanent record oftest results.

Leak rates, for the case of throughwall defects, can be calculated 6'om the number of pump strokes over a period of time.

Each pump stroke displaces 1.08 cu. in. (0.0047 gal.) ofwater.

The system can supply 1.0 gpm at 1000 psi which decreases to 0.5 gpm at 4700 psi.

C The above system was developed for testing primarily circumferential and short axial cracks.

A modification to the tool increased the hydro-chamber length to five inches, thereby permitting testing of axial cracks greater than five inches.

The axial crack system is basically the same as described above except the grippers have been eliminated.

2.3 Summary ofLocalized Tool Uses The original in-situ pressure test tool was designed to hydrostatically pressure test a short portion (approximately 3 inches) of a steam generator tube at the location of a defect (as opposed to

testing the fulllength), such that the resultant loading would be identical to that imposed during a capped hydrostatic test. The system can be used in one ofthree modes as foHows:

a)

H drostatic load testin, in which the tool is used to pressurize a three (3) inch length ofthe tube with proper axial tensile forces imparted to the tube from the test pressure.

The five inch chamber length provides proper hoop stresses only.

The objective is to demonstrate that the defective tube section is capable of sustaining a pressure ofat least three (3) times the normal operating pressure differential without rupture. In the absence ofthroughwall penetration, this is a static test.

b)

H drod namic leak rate testin, in which the tool is used to evaluate leak rates at various pressures for tubes with throughwall defects.

The system can deliver approximately 1 gpm of ambient temperature water at 1000 psi, decreasing to 0.5 gpm at 4700 psi.

')

H drostatic burst testin, which is used to test tubes with throughwall defects so large that pressures equal to three (3) times operating pressure differential cannot be attained because ofpump capacity limitations. In this test, the through-wall defect is covered with the upper seal bladder of the tool to limit through-wall leakage and then the tool is pressurized in the normal manner.

The pressure within the seal bladder will impart the proper hydrostatic level of hoop stress in the tube defect region while the gripper bladders (circumferential tool only) impart the proper hydrostatic level of axial tensile load.

This approach to pressure testing tubes with throughwall defects is consistent with the EPRI guidelines for conducting SG tube burst testing which requires the use ofa bladder to overcome throughwall leakage.

For the St. Lucie-1 SG tubes, there were several through-wall defects.

Thus, all three modes of testing were employed.

2.4 Summary of Qualification Testing The individual parts of the tool and the complete tool were tested in a variety of ways to demonstrate adequate performance of the tool.

The most important tests were conducted to demonstrate that the stresses (or strains) imposed by the in-situ test tool would be identical to those imposed by a capped tube hydrotest.

Test sections of3/4 inch OD by 0.048 inch wall Alloy 600 steam generator tubes were instrumented with biaxial stain gages which were positioned at the section mid-point and 180 degrees apart.

Strains were measured during a capped tube hydrostatic test and during a hydrostatic test using the in-situ pressure test system.

The results indicated that the strains imposed by the in-situ pressure test tool were the same as for the capped tube hydro test.

Reference 3 provides the details ofthe qualification tests for the localized in-situ test tool.

The tool described in Reference 3 was developed to pressure test primarily circumferentially oriented defects in the expansion transitions at the top of the tubesheet.

This too, although referred to as the "circumferential tool", may also be used for testing axial indications. An additional tool has evolved for testing of axial defects which are greater in length than those which can be tested in the original "circumferential tool". Since the tool design for the circumferential defects has greater restrictions than the tool for axial defects, the test report is bounding for the axial tool.

For the St. Lucie-1 testing, an additional set of tests were performed to further qualify the tools.

Reference 3 noted that for the case of a leaking SG tube, the pressure at the pump discharge and in the tube willbe different because of pressure losses for the water through the hoses.

Also, because ofthe cyclic operation ofthe pump, the pressure willfluctuate.

A specific configuration, not identical to St. Lucie-l, was tested for Reference 3 and Rom that testing the pressure in the tube could be estimated Gom the pump pressure for various leak rates.

Reference 3 noted that the results applied only to the configuration tested and willdiffer for other configurations.

For St. Lucie-l, longer hoses were required by the need to test defect indications in the upper bundle region of the SGs.

For non-leaking defects, the length of the hoses has no effect on the test chamber pressure.

However, for a leaking tube the pressure in the test chamber

could not be determined without additional testing.

Attachment A (Reference 4) describes the testing and provides the adjustments to be applied to pump pressures to insure test chamber pressures exceed the target pressures.

2.5 Test Condition Adjustments Reference 2 noted that the main issue ofinterpretation and application ofin-situ pressure test data is ascertaining their significance relative to regulatory requirements and to conditions incurred during normal operating or accident conditions. Guidelines for extrapolating test data to operating or accident conditions are contained in Reference 2 and were considered when developing the target pressures for the St. Lucie-1 tests.

Extrapolation of in-situ test results from ambient conditions where the testing occurs to service conditions requires a correction to account for temperature.

The average flow strength (average of yield and ultimate strengths) which governs burst pressures, decreases with increasing temperature.

To insure that the severity of loading during the test was equivalent to that in operation, the test pressures were increased by 13 percent.

The value is consistent with temperature adjustments in laboratory burst testing of steam generator tubes removed Gom operating plants (Reference 5, for example).

The value resulted Rom laboratory tests at ambient temperature and 6SO'F on non-defective steam generator tubes (Reference 6).

For axiaHy oriented free span cracks, only the hoop pressure stresses are of interest.

For tubes with circumferentially oriented defects, axial stresses must be applied across the degraded section.

The qualification testing summarized in section 2.4 indicated that the tool applied axial stresses equivalent to a capped tube hydrotest which would be consistent with service induced stresses.

As long as the tube is free to move axially during the test, there is no need for an additional correction factor.

The eggcrate supports and the tube support plates at St. Lucie-1 are carbon steel.

In many plants with carbon steel supports, corrosion of the carbon steel in the tube -to-support crevices has

resulted in corrosion product build-up to the point where tubes become locked (or frozen) at the supports.

The presence of this condition at St. Lucie-1 could not be discounted.

Accordmgly, the design of the in-situ test plan for St. Lucie-1 assumed that the tubes were locked at the tube supports.

For axially oriented cracks, only hoop stresses are important in assessing tube integrity, and thus, no connections need to be applied to in-situ test pressures to account for the effect of tubes locked at tube supports.

For circumferentially oriented cracks, axial stresses induced by the in-situ pressure test must be applied across the degraded section.

During the test, the tube will expand in the axial direction. Ifa tube is free to move axially through the supports, test results can be used without correction.

However, as a result ofsupport corrosion, the tubes being tested may become locked at the supports, thereby hindering axial tube displacements (in effect, reducing axial loads during the test, making the test results non-conservative).

References 2 and 7 noted calculations had been performed to determme axial stresses in tubes with axisymetric circumferential degradation for several different axial boundary conditions. Two general cases of interest were noted:

1) loading applied by a localized pressurized tool to produce an axial force in a locked, degraded tube surrounded by locked, non-degraded, non-pressurized adjacent tubes and 2) full length pressure loading of a locked, degraded tube surrounded by locked, non-degraded, non-pressurized adjacent tubes.

0 Reference 2 argues that Regulatory Guide 1.121 structural margins are adequately demonstrated when in-situ pressure test tooling provides an axial stress equivalent to the axial stress experienced by an in-service tube subjected to an internal pressure of3 times the normal operating pressure differential. The calculations summarized by Reference 2 and 7 indicate that a correction factor needs to be applied to the in-situ test pressure to create the same axial stress as experienced by an in-situ service tool.

The size of the correction factor is affected by the distances between tubesheet and support where locking has occurred and by the mechanical

properties (yield strength) of the tubes.,

The largest correction factors for localized in-situ pressure testing result for the shortest distances and the highest yield strengths.

A correction factor of 1.127 (increase in pressure of 12.7 percent) bounded all of the localized in-situ pressure test cases evaluated.

Reference 7 also described an analytical evaluation of a fulltube in-situ test ofa locked tube. The result for this test was a correction factor of 1.78, indicating that testing of a locked tube with circumferential cracking was ofmarginal value. Laboratory test comparison of locked and non-locked tubes (Reference 7) confirmed the reduction in axial loads for the locked tube, thereby indicating the need to increase the test pressures to insure that the test provided stress conditions at least as severe as those expected for an in-service tube.

Prior to testing at St. Lucie-l, ABB CENO determined a St. Lucie-1 specific correction factor to be applied to localized tests ofcircumferentially oriented defects.

For the case of 3/4 inch OD by 0.048 inch tubing, assuming tubes are locked at the first eggcrate support, this correction factor was 8.5% (pressure to be increased by factor of 1.085).

In summary, at St. Lucie-1 target test pressures were increased by:

a) 13 percent for axial and volumetric indications to correct for temperature b) 21.5% for circumferentially oriented indications to correct for temperature and for tubes locked at support locations.

To further insure that target pressures were attained, an additional 50 psi was added as a pressure gauge calibration correction.

Figure 2-1. Schematic ofIn-situ Pressure Test Tool.

10

Section 3.0 ST. LUCIE-1 TEST PROCEDURES In-situ pressure testing ofSt. Lucie-1 steam generator tubes was conducted in accordance with ABB CENO Procedure STD-100-204, Rev. 9, "Procedure for the Checkout and Operation ofthe Steam Generator Tube In-Situ Hydrostatic Test Tool" and Traveler No. PSL-007 Rev. 6, "In-Situ Hydro Test Traveler". Atotal of 17 tubes were tested.

14 with a localized tool and 3 with the fulltube hydro equipment.

The tubes had a variety ofdefect types including upper bundle Iree span axial indications, (b) top-of-the-tubesheet circumferential indications, (c) axial indications just above the tubesheet (sludge pile region), (d) axial indications at eggcrate locations, (e) axial indications at drilled support plates and (f) volumetric indications at drilled support plates.

FPL selected the tubes for testing based on ECT results.

The ECT data are included in Table 4-1 which summarizes the test results.

The tubes selected for testing were:

a) upper bundle free span axial indications by fulltube hydro:

SGA R89L107 - several free span indications SGA R33L109 - several free span indications SGA R42L128 - largest voltage by MRPC b) circumferential indications at the top ofthe tubesheet SGA R13L113 - cold leg side, maximum voltage by MRPC SGB R40L98

- hot leg side, maximum percent degraded area SGB '90L38

- hot leg side c) axial indications just above the top ofthe tubesheet (sludge pile area)

SGB R29L47

- deepest bobbin coil indicated flaw

SGB R78L84

- bobbin coil highest voltage SGB R88L44

- worst case indication which could be left in service SGB R33L115 - maximum depth volumetric indication, d) axial indications at eggcrate locations SGB SGB SGB R83L97

- major growth in defect size R99L119 - highest voltage indicated by bobbin coil R15L55

- deepest flaw indicated by bobbin coil e) axial and volumetric indications at the lower partial drilled support plate SGB SGB SGB

, SGB R105L1 03 - highest voltage indicated by bobbin coil R109L81

- 7th deepest axial indication by bobbin coil R104L70

- NDD by bobbin coil, volumetric indication by MRPC Rl 14L106 - highest voltage volumetric indication by bobbin coil FPL provided the target test pressures, as adjusted for temperature (13% increase) axial load correction factor for tubes locked at supports (8.5% increase) and 50 psig added for pressure gauge calibration correction. The corrected target pressures for each defect type were:

D~efect T e

Corrected Target Condition Pressure, psi Axial&volumetric Normal operating d,P 1672 indications Main steam line break 3 times NObP 2875 4915 Circumferential indications Normal operating b,F Main steam line break 3 times NOBP 1794 3088 5281 12

Prior to conducting a localized test, the in-situ pressure test tool was positioned in the tubesheet region ofthe tube and was then pressurized to three times normal operating pressure differential to verifythat the tool was operating and to identify and measure any leakage past the bladders.

The pressure was maintained for one minute. Afterverifying operability and the absence of bladder by-pass, the tool was re-positioned so that the defect region was covered by the hydro-test chamber ofthe tool. The defect area ofeach tube was then pressure tested in accordance with the foHowing schedule:

l)

The defect area ofthe tube was pressurized to the adjusted normal operating pressure differential and the pressure was maintained for five minutes to observe for leakage.

Had there been any leakage, a leak test offive minutes duration would have been conducted to determine a leak rate.

2)

The defect area ofthe tube was then pressurized to the adjusted main steam line break pressure and held at that pressure for five minutes to observe for leakage and determine a leak rate. As discussed in the following section, one tube did not reach the target pressure because leakage developed at a lower pressure and exceeded pump capacity at a pressure less than MSLB. For leaking tubes, the pressure was decreased to normal operating pressure differential of five minutes for a leak rate determination after exposure to MSLB pressures.

3)

The defect area ofthe tube was pressurized to 3 times adjusted normal operating pressures for five minutes.

For specimens with leakage which prevented attaining the target pressures, the tool was repositioned so that the defect area was covered by the upper bladder and the tool re-pressurized to the target pressure.

For the fulltube tests, the tube ends were plugged with the appropriate tools and the tube was pressurized in accordance with the same schedule as was used for the localized testing.

13

Section 4.0 RESULTS Table 4-1 summarizes the fulltube and localized in-situ pressure test results for the St. Lucie-I steam generators.

The table provides tube identification, flaw type, size and location, ECT data, target pressures, maximum pressures attained and leak rates at the various pressures.

There were not any catastrophic failures (burst) of any of the defective St. Lucie-1 tubes tested, even when pressurized to pressures of 3 times normal operating pressure differentials (3 NOBZ)

(adjusted for temperature and tube lock-up).

The three tubes with axial free span flaws did not develop leakage at test pressures up to 5000 psi although the flaws were long (up to 7.0 inches) and deep (100% throughwall, 88% degraded area) as indicated by MRPC testing.

The three tubes with circumferential crack indications at the top of the tubesheet survived pressures of 5300 to 5325 psi without developing leakage.

The MRPC indicated depths and calculated percent degraded areas for these tubes were up to 86% and 55%, respectively.

Two of the four tubes with sludge pile axial defects survived test pressures of 4950 - 5000 psi without leakage developing.

Tube R29L47 developed leakage during pressurization to adjusted MSLB pressures (2900 psi) which was measured at 0.26 gpm.

When pressure was decreased to adjusted normal operating pressure differential (NOB,P) the leak decreased to 0.12 gpm.

The defect was covered with a bladder for the final step oftesting, but the bladder developed leakage at 4300 psi.

However, leakage from the bladder was sufficiently small that the target pressure was achieved.

A second tube (R78L84) developed a leak at 4400 psi but with the aid of a bladder, the target pressure was achieved.

Two of the three axial eggcrate fiaws developed leaks during testing.

Tube R83L79 began leaking at 2400 psi.

Leak measurements were conducted at 2150 psi bladder pressure which attachment A indicates would equal a pressure of 1750 psi in the test chamber.

A post leak rate 14

attempt to attain MSLB pressure was not successful.

Subsequent leak rate measurements at NObP produced a 0.40 gpm result which suggests some plastic deformation ofthe defect.

When a bladder was used to cover the defect, the highest target pressure was attained without incident.

The second leaking tube (R15L55) did not leak when first tested at NOAP but did have a small leak (0.02 gpm) at adjusted MSLB pressure.

When pressure was decreased to NOAP, the leak rate decreased to 0.01 gpm.

With the aid of a bladder over the defect, the maximum target pressure was achieved.

There was not any measurable leakage during test ofthe four tubes with defect indications at the 09H partial drilled support plate.

15

ST. LUCIE-1 IN-SITUPRESSURE TEST RESULTS Stcam. Gen.

Region TUBE INFORMATION MRPC DATA BOBBINDATA IN-SITUTEST/

LEAKAGEDATA Row Line Location Length Volts Max %

PDA Ax/Circ Volts Max/o GPM O

NOPD GPM e

htSLB GPht Q NOPD POST MSLB Pressure 3xYOPD

'STEAM GE5ERATORA Circ. Flaws Free Span Free Span Free Span Free Span 13 89 89 33 42 113 TSC+0.1 107 8H+12.0 107 8H+10.8 109 6H+17-19 128 6H+10.63 1.80 2.50 7.00 5.1 4.8 9.60 2.00 1.80 1.61

, 1.75

'STEAM 78 37 CSI 100 80 ASI 99 88 ASI 84 61 ASI 100 94 ASI RATOR'A NA 0.20 NDD 0

NDD 0

NDD 0

29 NDD 0

NA 5300 NA 5000 NA 5000 NA 5000 NA 4950 Circ. Flaw Circ. Flaw 40 90 1.40 38 TSH+0.1 98 TSH+0.1 2.00 2.13 1.97 77 55 CSI 86 37 CEI NA NDD 0

NDD 0

NA 5300 NA 5325 Sludge Pile Sludge Pile Sludge Pile Sludge Pile Eggcrate 29 78 88 33 83 47 TSH+5.3 0.40 84 TSH+0.8 0.64 44 TSH+1.5 0.54 97 1H 0.96 115 TSH+5.7 0.53 7.80 3.37 1.35 0.92 10.80 97 76 ASI 49 48 ASI 62 50 ASI 44 NA VOL 86 76 ASI 5.00 7.60 3.00 1.50 5.60 81 56 28 69 81 0>

0.26 0.25 0.12 1 5000 NA 5000 NA 5000 NA 4950 0.40 (3)5100 Eggcratc Eggcrate Drilled Sup.

Drilled Sup.

Drilled Sup.

Drilled Sup.

15 105 114 109 104 119 55 103 106 81 70 1H 1H 9H 9H 9H 9H 0.73 0.90 0.72 NA 0.46 NA 10.00 12.30 7.20 3.80 1.80 2.20 90 75 ASI 90 67 ASI 51 28 ASI 37 NA VOL 69 53 ASI 81 NA VOL 6.60 5.60 2.60 7.00 1.30 11.6 80 94/64 0

79 20 52 DNT 0

0.02 NA (2 5000 0.01 (3)5000 NA 5000 NA 5000 NA 5000 NA 4950 (1)

Max. pressure achieved.

Bladder failed at 4300 psi.

(2)

Burst with bladder over flaw. < 0.25 GPM @4800 psi without bladder.

(3)

With burst bladder over flaw.

16

Section

5.0 CONCLUSION

S The seventeen St. Lucie-1 tubes that were in-situ pressure tested with the localized tools or by the fulltube technique met the most limitingrequirement ofUSNRC Regulatory Guide 1.121, that being that defective tubes must be able to withstand without burst a pressure ofthree times the normal operating pressure differential.

17

Section

6.0 REFERENCES

1.

USNRC Regulatory Guide 1.121 (Draft), "Bases for Plugging Degraded PWR Steam Generator Tubes," August, 1976 2.

EPRI Guidelines for In-Situ Pressure Testing ofSteam Generator Tubes 3.

B.F. Allen, "Final Report for the Steam Generator Tube In-Situ Hydrostatic Test Tool,"

TR-ESE-1030, Rev. 00, April 1, 1994 4.

R.M. Orsulak, "Test Report Steam Generator Tube In-Situ Hydrostatic Pressure Test Tool Hydro Chamber Pressure Determination, "TR-9419-CSE-96-1101, Rev. 0," June 12, 1996 5.

T.P. Magee and J.F. Hall, "Examination ofTrojan Steam Generator Tubes Volume 1 Examination Results,"

EPRI TR-101427, November, 1992 6.

"Steam Generator Tube Degradation at the Support Plates, CEOG Task 729," CE NPSD 957, October, 1994 7.

"Steam Generator Tube In-Situ Pressure Testing Guidelines CEOG Task 844," CE NPSD-1005-P, June 1995 18