ML16032A095

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IR 05000277/2015004 and 05000278/2015004: Peach Bottom Atomic Power Station - Integrated Inspection Report (October 1 - December 31, 2015)
ML16032A095
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 02/01/2016
From: Daniel Schroeder
Reactor Projects Region 1 Branch 4
To: Bryan Hanson
Exelon Nuclear
SCHROEDER, DL
References
IR 2015004
Download: ML16032A095 (43)


See also: IR 05000277/2015004

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION I

2100 RENAISSANCE BLVD., SUITE 100

KING OF PRUSSIA, PA 19406-2713

February 1, 2016

Mr. Bryan Hanson

Senior Vice President, Exelon Generation Company, LLC

President and Chief Nuclear Officer, Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT:

PEACH BOTTOM ATOMIC POWER STATION - INTEGRATED INSPECTION

REPORT 05000277/2015004 AND 05000278/2015004

Dear Mr. Hanson:

On December 31, 2015, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Peach Bottom Atomic Power Station (PBAPS), Units 2 and 3. The enclosed

inspection report documents the inspection results, which were discussed on January 15, 2016,

with Mr. Pat Navin, Peach Bottom Plant Manager, and other members of your staff.

NRC Inspectors examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

The inspectors documented one finding of very low safety significance (Green) in this report.

This finding involved a violation of NRC requirements. The NRC is treating this violation as a

non-cited violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the NCV in this report, you should provide a response within 30 days of the date

of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region I; the Director, Office of Enforcement, United States Nuclear Regulatory

Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at PBAPS.

B. Hanson

- 2 -

In accordance with Title 10 of the Code of Federal Regulations (CFR) 2.390 of the NRC's

"Rules of Practice," a copy of this letter, its enclosure, and your response (if any), will be

available electronically for public inspection in the NRCs Public Document Room or from

the Publicly Available Records component of the NRC's Agencywide Documents Access

and Management System (ADAMS). ADAMS is accessible from the NRC website at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Daniel L. Schroeder, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket Nos.

50-277 and 50-278

License Nos. DPR-44 and DPR-56

Enclosure:

Inspection Report 05000277/2015004 and 05000278/2015004

w/Attachment: Supplementary Information

cc w/encl: Distribution via ListServ

ML16032A095

SUNSI Review

Non-Sensitive

Sensitive

Publicly Available

Non-Publicly Available

OFFICE RI/DRP

RI/DRP

R1/DRP

NAME JHeinly/ DLS by telecon

ATurilin/ AT

DSchroeder/ DLS

DATE

01/28 /16

01/28 /16

02/01/16

1

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket Nos.

50-277 and 50-278

License Nos.

DPR-44 and DPR-56

Report No.

05000277/2015004 and 05000278/2015004

Licensee:

Exelon Generation Company, LLC

Facility:

Peach Bottom Atomic Power Station, Units 2 and 3

Location:

Delta, Pennsylvania

Dates:

October 1, 2015 through December 31, 2015

Inspectors:

B. Smith, (Acting) Senior Resident Inspector

L. Micewski, (Acting) Senior Resident Inspector

B. Reyes, (Acting) Senior Resident Inspector

J. Patel, (Acting) Resident Inspector

S. Barber, Senior Project Engineer

N. Floyd, Reactor Inspector

C. Graves, Health Physicist

C. Highley, Project Engineer

D. Kern, Senior Reactor Inspector

M. Modes, Reactor Inspector

D. Orr, Senior Reactor Inspector

A. Turilin, Project Engineer

Approved By:

Daniel L. Schroeder, Chief

Reactor Projects Branch 4

Division of Reactor Projects

2

TABLE OF CONTENTS

SUMMARY ................................................................................................................................. 3

1. REACTOR SAFETY ................................................................................................................ 4

1R01

Adverse Weather Protection ...................................................................................... 4

1R04

Equipment Alignment ................................................................................................. 5

1R05

Fire Protection .......................................................................................................... 6

1R07

Heat Sink Performance ............................................................................................. 7

1R08

In-service Inspection Activities ................................................................................... 7

1R11

Licensed Operator Requalification Program and Licensed Operator Performance..... 9

1R12

Maintenance Effectiveness ...................................................................................... 10

1R13

Maintenance Risk Assessments and Emergent Work Control ................................ 10

1R15

Operability Determinations and Functionality Assessments ..................................... 11

1R18

Plant Modifications ................................................................................................... 11

1R19

Post-Maintenance Testing ...................................................................................... 12

1R20

Refueling and Other Outage Activities .................................................................... 13

1R22

Surveillance Testing ............................................................................................... 14

1EP6

Drill Evaluation ........................................................................................................ 14

2. RADIATION SAFETY ............................................................................................................ 17

2RS1

Radiological Hazard Assessment and Exposure Controls ....................................... 17

2RS2

Occupational ALARA Planning and Controls .......................................................... 18

2RS3

In-Plant Airborne Radioactivity Control and Mitigation ............................................. 19

2RS5

Radiation Monitoring Instrumentation ...................................................................... 20

2RS6

Radioactive Gaseous and Liquid Effluent Treatment ............................................... 21

4. OTHER ACTIVITIES ............................................................................................................. 21

4OA1

Performance Indicator Verification .......................................................................... 21

4OA2

Problem Identification and Resolution ..................................................................... 22

4OA3

Follow-Up of Events and Notices of Enforcement Discretion .................................. 26

4OA5

Other Activities ....................................................................................................... 26

4OA6

Meetings, Including Exit ........................................................................................... 26

SUPPLEMENTARY INFORMATION ....................................................................................... A-1

KEY POINTS OF CONTACT .................................................................................................. A-1

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED .................................... A-1

LIST OF DOCUMENTS REVIEWED ....................................................................................... A-2

LIST OF ACRONYMS ........................................................................................................... A-12

3

SUMMARY

IR 05000277/2015004, 05000278/2015004, 10/01/2015 - 12/31/2015; Peach Bottom Atomic

Power Station (PBAPS), Units 2 and 3; Surveillance Testing.

This report covered a three-month period of inspection by resident inspectors, and announced

baseline inspections performed by regional inspectors. The inspectors identified one non-cited

violation (NCV), which was of very low safety significance (Green). The significance of most

findings is indicated by their color (i.e., greater than Green, or Green, White, Yellow, Red) and

determined using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

(SDP), dated June 2, 2011. Cross-cutting aspects are determined using IMC 0310, Aspects

Within Cross-Cutting Areas, dated December 19, 2013. All violations of NRC requirements are

dispositioned in accordance with the NRCs Enforcement Policy, dated July 09, 2013. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, Reactor Oversight Process, Revision 5.

Cornerstone: Mitigating Systems

Green. The inspectors identified a non-cited violation (NCV) of very low safety significance

of 10 Code of Federal Regulations (CFR) Part 50, Appendix B, Criterion III, Design

Control, for not ensuring that the adequacy of PBAPS emergency diesel generator (EDG)

lubrication oil (LO) supply was designed to withstand the effects of natural phenomena.

Specifically, additional LO, evaluated by PBAPS to meet their EDG technical specification

(TS) mission time of seven days of continuous operation, was housed in a non-class I

structure that would be unable to withstand the effects of natural phenomena. PBAPS

entered the issue into the correction action program (CAP) as issue report (IR) 02603369

and took immediate corrective actions to relocate the LO reserve inventory from their

warehouse to the 135 elevation of the PBAPS radwaste building, which is a seismic class I

structure

The finding is considered more than minor because it is associated with the Protection

Against External Factors attribute of the Reactor Safety Mitigating Systems cornerstone and

adversely affected the cornerstones objective of ensuring reliability and capability of

systems that respond to initiating events to prevent undesirable consequences (i.e., core

damage). The inspectors evaluated the significance of this finding using IMC 0609

Appendix A, The SDP for Findings at Power, Exhibit 2, Mitigating Systems Screening

Questions. The inspectors determined that this finding was of very low safety significance

(Green) because the finding is a design deficiency which did not result in an actual loss of

functionality of the EDGs. This finding did not have a cross-cutting aspect because the most

significant contributor of the performance deficiency (PD) occurred during the 1994

conversion to improved technical specifications (ITS) and, thus, was not reflective of current

plant performance. Specifically, PBAPS current engineering change request (ECR)

process would evaluate for natural phenomena considerations such as seismic, tornado,

flood, etc. (Section 1R22)

Other Findings

None.

4

REPORT DETAILS

Summary of Plant Status

Unit 2 began the inspection period at 100 percent rated thermal power (RTP). On

December 13, 2015, Unit 2 commenced a shutdown from 100 percent RTP and entered into

a forced outage to repair packing on the 2 C inboard main steam isolation Valve (MSIV). On

December 15, 2015, the Unit 2 reactor mode switch was placed in start-up and the main

generator was synchronized to the electrical grid on December 17, 2015. On December 18,

2015, Unit 2 was returned to 100 percent RTP, and remained at 100 percent RTP until the end

of the inspection period.

Unit 3 began the inspection period in a refueling outage (RFO) (P3R20). On October 21, 2015,

the Unit 3 reactor mode switch was placed in start-up and the main generator was synchronized

to the electrical grid on October 22, 2015. On October 25, 2015, Unit 3 was returned to

89 percent power (the pre-extended power uprate (EPU) 100 percent power limit). On

November 24, 2015, Unit 3 down powered from 92 percent RTP to 77 percent RTP to perform

breaker maintenance on the 3 A condensate pump. Unit 3 returned to 92 percent RTP later

that same day. On December 3, 2015, Unit 3 raised power to the full 100 percent RTP EPU

limit after final NRC approval for power ascension. Unit 3 remained at 100 percent RTP until

the end of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01 - 2 samples)

.1

Readiness for Impending Adverse Weather Conditions (1 sample)

a. Inspection Scope

The inspectors reviewed PBAPS preparations for the onset of a thunderstorm on

October 2, 2015, resulting from Hurricane Joaquin. The inspectors reviewed the

implementation of PBAPS' adverse weather preparation procedures before the onset

of the adverse weather condition. The inspectors walked down the north substation,

EDGs, and output transformer yard system availability. The inspectors verified that

operator actions defined in PBAPS adverse weather procedure maintained the

readiness of essential systems. The inspectors discussed readiness and staff

availability for adverse weather response with operations and work control personnel.

Documents reviewed for each section of this inspection report are listed in the

Attachment.

b. Findings

No findings were identified.

5

.2

Winter Readiness - Seasonal Extreme (1 sample)

a. Inspection Scope

The inspectors reviewed PBAPS readiness for the cold weather preparations on

December 11, 2015. The review focused on the EDGs, the river water intake structure

travelling screens, emergency cooling tower (ECT), circulating water pump house, and

associated support equipment. The inspectors reviewed the Updated Final Safety

Analysis Report (UFSAR), TSs, and the CAP to determine the temperatures or other

seasonal weather conditions that could challenge these systems. The review ensured

PBAPS personnel had prepared adequately for the weather-related challenges. The

inspectors reviewed station procedures, including PBAPS seasonal weather preparation

procedure, and applicable operating procedures. The inspectors performed walkdowns

of the selected systems to ensure station personnel identified issues that could challenge

the operability of the systems during cold weather conditions.

b. Findings

No findings were identified.

1R04 Equipment Alignment (71111.04 - 3 samples)

.1

Partial System Walkdowns (71111.04Q - 2 samples)

a. Inspection Scope

The inspectors performed partial walkdowns of the following systems:

Unit 3 B residual heat removal (RHR) following the cross-tie modification on

October 20, 2015

Unit 3 reactor core isolation cooling (RCIC) following restoration after the RFO on

October 21, 2015

The inspectors selected these systems based on their risk-significance relative to the

Reactor Safety cornerstones at the time they were inspected. The inspectors reviewed

applicable operating procedures, system diagrams, the UFSAR, TSs, work orders

(WOs), IRs, and the impact of ongoing work activities on redundant trains of equipment

in order to identify conditions that could have impacted the systems performance of its

intended safety functions. The inspectors also performed field walkdowns of accessible

portions of the systems to verify system components and support equipment were

aligned correctly and were operable. The inspectors examined the material condition

of the components and observed operating parameters of equipment to verify that there

were no deficiencies. The inspectors also reviewed whether PBAPS staff had properly

identified equipment issues and entered them into the CAP for resolution with the

appropriate significance characterization.

b. Findings

No findings were identified.

6

.2

Full System Walkdown (71111.04S - 1 sample)

a. Inspection Scope

During the week of September 28, 2015, the inspectors performed a complete system

walkdown of accessible portions of the Unit 3 automatic depressurization system and

associated Unit 3 safety relief valves (SRVs) to verify the existing equipment lineup was

correct. The inspectors reviewed operating procedures, surveillance tests (STs),

drawings, equipment line-up check-off lists, and the UFSAR to verify the system was

aligned to perform its required safety functions. The inspectors also reviewed electrical

power availability, component lubrication and equipment cooling, hanger and support

functionality, and operability of support systems. The inspectors performed field

walkdowns of accessible portions of the system to verify as-built system configuration

matched plant documentation, and that system components and support equipment

remained operable. The inspectors confirmed that systems and components were

aligned correctly, free from interference from temporary services or isolation boundaries,

environmentally qualified, and protected from external threats. The inspectors also

examined the material condition of the components for degradation and observed

operating parameters of equipment to verify that there were no deficiencies.

Additionally, the inspectors reviewed a sample of related IRs and WOs to ensure PBAPS

appropriately evaluated and resolved any deficiencies.

b. Findings

No findings were identified.

1R05 Fire Protection (71111.05Q - 5 samples)

Resident Inspector Quarterly Walkdowns

a. Inspection Scope

The inspectors conducted tours of the areas listed below to assess the material

condition and operational status of fire protection features. The inspectors verified

that PBAPS controlled combustible materials and ignition sources were controlled in

accordance with administrative procedures. The inspectors verified that fire protection

and suppression equipment was available for use as specified in the area pre-fire plan,

and passive fire barriers were maintained in good material condition. The inspectors

also verified that station personnel implemented compensatory measures for out-of-

service (OOS), degraded or inoperable fire protection equipment, as applicable, in

accordance with procedures.

Unit 3 recirculation pump motor generator (MG) set room and adjustable speed drive

(ASD) trailer on October 1, 2015

Unit 3 torus space on October 19, 2015

Unit 3 outboard MSIV room on October 20, 2015

Units 2 and 3 cable spreading room on October 30, 2015

Units 2 and 3 main control room on November 5, 2015

7

b. Findings

No findings were identified.

1R07 Heat Sink Performance (71111.07A - 1 sample)

a. Inspection Scope

The inspectors reviewed the Unit 2 A RHR/high pressure service water (HPSW) heat

exchanger (HX) during the week of November 2, 2015, to determine its readiness and

availability to perform is safety functions. The inspectors reviewed the design basis for

the component and verified PBAPS commitments to NRC Generic Letter 89-13,

Service Water System Requirements Affecting Safety-Related Equipment. The

inspectors reviewed the results of the most recent thermal performance monitoring test

(performed February 12, 2015), the most recent internal visual inspection, including tube

sheet partition plate inspection and eddy current testing (performed February 12, 2015),

and trend assessment based on comparison with previous inspections and performance

tests. The inspectors discussed the results of the most recent inspection with

engineering staff. The inspectors verified that PBAPS initiated appropriate corrective

actions for identified deficiencies. The inspectors also verified that the number of tubes

plugged within the HX did not exceed the maximum amount allowed.

b. Findings

No findings were identified.

1R08 In-service Inspection Activities (71111.08 - 1 sample)

a. Inspection Scope

The inspectors reviewed Exelon staff implementation of in-service inspection (ISI)

program activities for monitoring degradation of the reactor coolant system boundary,

risk significant piping and components, and containment systems during the PBAPS

Unit 3 20th RFO. The inspection was completed onsite September 21 to 28, 2015,

followed by in-office review October 8 to 9, 2015. The sample selection for this

inspection was based on the inspection procedure objectives and risk priority of those

pressure retaining components in systems where degradation would result in a

significant increase in risk. The inspectors observed in-process non-destructive

examinations (NDE), reviewed documentation, and interviewed Exelon personnel to

verify that the NDE activities performed as part of the fourth interval, third period, of the

Peach Bottom Unit 3 ISI program were conducted in accordance with the requirements

of the American Society of Mechanical Engineers (ASME) Boiler and Pressure Vessel

Code,Section XI, 2001 Edition with 2002 and 2003 Addenda.

NDE and Welding Activities

The inspectors performed direct observation of NDE activities in process and reviewed

documentation of completed examinations listed below. Activities included review of

ultrasonic testing (UT), radiographic testing (RT), and visual examination (VT).

8

The inspectors reviewed certifications of the NDE technicians performing the

examinations and verified that the inspections were performed in accordance with

approved NDE procedures and industry guidance. For UT activities, the inspectors also

verified the calibration of equipment used to perform the examinations. The inspectors

verified that the test results were reviewed and evaluated by certified Level III NDE

personnel and that the parameters used in the test were in accordance with the

limitations, precautions, and prerequisites specified in the test procedure.

ASME Code Required Examinations:

Direct observation of the manual UT of the N4E nozzle-to-vessel weld in the

feedwater system.

Direct observation of the manual UT of the N4E nozzle inner radius and bore in the

feedwater system.

Documentation review of the manual UT of the reactor pressure vessel closure head

studs (Studs 47-92).

Documentation review of the RT of two pipe-to-flange welds (10-2XC020-11 and -12)

and one pipe-to-pipe weld (10-2DC20-29), 20-inch diameter, performed as part of a

modification activity in the RHR system.

Direct observation of the VT of the drywell (i.e., containment) interior and exterior

penetrations and surfaces. The inspectors independently examined the condition of

the drywell interior liner surfaces at all floor elevations, including the moisture barrier

at the 11911 elevation. The inspectors performed a documentation review of the

drywell VT records and compared those to the inspector walkdowns.

Review of Previous Indications Accepted by Evaluation

The inspectors did not review any previous indications because there were no relevant

indications from the previous outage that required evaluation for continued service.

Repair/Replacement Activities Including Welding Activities

The inspectors reviewed the modification package associated with engineering change

11-00376, which implemented plant changes as part of the EPU project. Specifically,

the scope of the modification was to install a piping cross-tie between the Unit 3 A and

C trains of the RHR system in order to increase the containment cooling capability

following a postulated design basis event.

The inspectors performed a direct observation of the welding activities associated with

two piping welds (10-2XC020-11 and -12) in progress and performed a documentation

review of one completed weld (10-2DC20-29) to verify that welding and applicable NDE

activities were performed in accordance with ASME code requirements. The inspectors

reviewed the weld procedure and weld information data sheet, and also reviewed the

radiography data sheets for final acceptance of the welds. The modification was

performed under WOs C0255830 and C0255936.

9

Identification and Resolution of Problems

The inspectors reviewed a sample of PBAPS Unit 3 corrective action reports, which

identified NDE indications, deficiencies, and other non-conforming conditions since the

previous RFO and during the current outage. The inspectors verified that non-

conforming conditions were properly identified, characterized, evaluated, and that

corrective actions were identified and entered into the CAP for resolution.

b. Findings

No findings were identified.

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11Q - 3 samples)

.1

Quarterly Review of Licensed Operator Requalification Testing and Training (1 sample)

a. Inspection Scope

The inspectors observed a licensed operator requalification training scenario for the site

area on November 9, 2015. The inspectors evaluated operator performance during the

simulated event and verified completion of risk significant operator actions, including the

use of abnormal and emergency operating procedures. The inspectors assessed the

clarity and effectiveness of communications, implementation of actions in response to

alarms and degrading plant conditions, and the oversight and direction provided by the

control room supervisor. The inspectors verified the accuracy and timeliness of the

emergency classifications made by the shift manager and the TS action statements

entered by the shift technical advisor. Additionally, the inspectors assessed the ability of

the crew and training staff to identify and document crew performance problems.

b. Findings

No findings were identified.

.2

Quarterly Review of Licensed Operator Performance in the Main Control Room

(2 samples)

a. Inspection Scope

The inspectors observed and reviewed the licensed operator performance from the main

control room during the reactivity evolutions listed below. The inspectors observed use

of and compliance with procedures, crew communications, interpretation, diagnosis,

and understanding of plant alarms, use of human error prevention techniques,

documentation of activities, and management oversight of the evolution to verify that

the crew was following procedures and plant expectations for conduct of operations.

Unit 3 plant startup and heat up from RFO 3R20 on October 20 and 21, 2015

Unit 2 plant shutdown and cooldown for a forced outage to repair a packing leak on

the C inboard MSIV on December 13, 2015

10

b. Findings

No findings were identified.

1R12 Maintenance Effectiveness (71111.12Q - 1 sample)

a. Inspection Scope

The inspectors reviewed the samples listed below to assess the effectiveness of

maintenance activities on structures, systems, and components (SSCs) performance

and reliability. The inspectors reviewed system health reports, CAP documents,

maintenance WOs, and maintenance rule (MR) basis documents to ensure that

PBAPS was identifying and properly evaluating performance problems within the scope

of the MR. For each sample selected, the inspectors verified that the SSC was properly

scoped into the MR in accordance with 10 CFR 50.65 and that the (a)(2) performance

criteria established by the PBAPS staff were reasonable. As applicable, for SSCs

classified as (a)(1), the inspectors assessed the adequacy of goals and corrective

actions to return these SSCs to (a)(2) status. Additionally, the inspectors ensured that

PBAPS staff was identifying and addressing common cause failures that occurred within

and across MR system boundaries.

Unit 3 recirculation system and ASDs on November 4, 2015

b. Findings

No findings were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13 - 3 samples)

a. Inspection Scope

The inspectors reviewed station evaluation and management of plant risk for the

maintenance and emergent work activities listed below to verify that PBAPS performed

the appropriate risk assessments prior to removing equipment for work. The inspectors

selected these activities based on potential risk significance relative to the Reactor

Safety cornerstones. As applicable for each activity, the inspectors verified that PBAPS

personnel performed risk assessments as required by 10 CFR 50.65(a)(4) and that the

assessments were accurate and complete. When PBAPS performed emergent work,

the inspectors verified that operations personnel promptly assessed and managed plant

risk. The inspectors reviewed the scope of maintenance work and discussed the results

of the assessment with the stations probabilistic risk analyst to verify plant conditions

were consistent with the risk assessment. The inspectors also reviewed the TS

requirements and inspected portions of redundant safety systems, when applicable, to

verify risk analysis assumptions were valid and applicable requirements were met.

Elevated risk, Unit 3 operation with a potential for draining the reactor vessel

(OPDRV) during local power range monitor swaps on October 1, October 5, and

October 6, 2015

Elevated risk, Unit 2 E-43 bus outage on October 13, 2015

Elevated risk, Unit 3 containment not fully inerted during plant startup on October 21,

2015

11

b. Findings

No findings were identified.

1R15 Operability Determinations and Functionality Assessments (71111.15 - 6 samples)

a. Inspection Scope

The inspectors reviewed operability determinations (ODs) for the following degraded or

non-conforming conditions based on the risk significance of the associated components

and systems:

Unit 3 standby liquid control (SBLC) test in which an explosive (squib) valve did not

appear to fire correctly on October 8, 2015

Unit 3 reactor water cleanup class 1 piping below minimum wall thickness on

October 8, 2015

Unit 3 MSIV snubbers low oil identified in reservoirs on October 9, 2015

Unit 3 D HPSW outlet valve tripped on torque switch on October 22, 2015

Unit 3 high-pressure coolant injection (HPCI) drain valve leaking by on October 22,

2015

Operator workarounds (OWAs) on November 5, 2015

The inspectors evaluated the technical adequacy of the ODs to assess whether TS

operability was properly justified and the subject component or system remained

available such that no unrecognized increase in risk occurred. The inspectors compared

the operability and design criteria in the appropriate sections of the TSs and UFSAR to

PBAPS evaluations to determine whether the components or systems were operable.

The inspectors confirmed, where appropriate, compliance with bounding limitations

associated with the evaluations, including compliance with in-service testing

requirements. Where compensatory measures were required to maintain operability,

such as in the case of OWAs, the inspectors determined whether the measures in place

would function as intended and were properly controlled by PBAPS. Based on the

review of selected OWAs listed above, the inspectors verified that PBAPS identified

OWAs at an appropriate threshold and addressed them in a manner that effectively

managed OWA-related adverse effects on operators and SSCs.

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18 - 1 sample)

Permanent Modification

a. Inspection Scope

The inspectors evaluated the following modification listed below:

Unit 3 reactor recirculation pump and ASDs modification on November 2 to

November 5, 2015

12

The inspectors verified that the design bases, licensing bases, and performance

capability of the affected systems were not degraded by the modifications. In addition,

the inspectors reviewed modification documents associated with the upgrade and design

change. The inspectors also reviewed 10 CFR 50.59 documentation, post-modification

testing results, procedure revisions, training documentation, and conducted field

walkdowns of the modifications.

b. Findings

No findings were identified

1R19 Post-Maintenance Testing (71111.19 - 9 samples)

a. Inspection Scope

The inspectors reviewed the post-maintenance tests (PMTs) for the maintenance

activities listed below to verify that procedures and test activities tested the safety

functions that may have been affected by the maintenance activity, that the acceptance

criteria in the procedure were consistent with the information in the applicable licensing

basis and/or design basis documents, and that the test results were properly reviewed

and accepted and problems were appropriately documented. The inspectors also

walked down the affected job site, observed the pre-job brief and post-job critique where

possible, confirmed work site cleanliness was maintained, and witnessed the test or

reviewed test data to verify quality control hold points were performed and checked, and

that results adequately demonstrated restoration of the affected safety functions.

Unit 3 A core spray (CS) valve local leak rate test (LLRT) following valve

maintenance on October 4, 2015

Unit 3 HPCI vacuum relief valves LLRTs following maintenance on October 5, 2015

Unit 3 A inboard MSIV LLRT following rework after failed LLRT on October 7, 2015

Unit 3 A HPSW following flex modifications on October 13, 2015

Unit 3 RCIC overspeed trip test following maintenance outage on October 15, 2015

Unit 3 A RHR PMT following crosstie modification on October 19, 2015

Unit 3 emergency auxiliary transformer following maintenance outage on November

19, 2015

Unit 3 B reactor feed pump PMT following maintenance on November 20, 2015

Unit 2 C inboard MSIV stroke timing following repacking on December 16, 2015

b. Findings

No findings were identified.

13

1R20 Refueling and Other Outage Activities (71111.20 - 2 samples)

.1

Unit 3 Refueling Outage (3R20) (1 sample)

a. Inspection Scope

The inspectors reviewed the stations work schedule and outage risk plan for the Unit 3

maintenance and RFO (3R20), conducted September 21 to October 20, 2015. The

inspectors reviewed Exelons development and implementation of outage plans and

schedules to verify that risk, industry experience, previous site-specific problems, and

defense-in-depth were considered. During the outage, the inspectors observed portions

of the shutdown and cooldown processes and monitored controls associated with the

following outage activities:

Configuration management, including maintenance of defense-in-depth,

commensurate with the outage plan for the key safety functions and compliance with

the applicable TSs when taking equipment OOS

Implementation of clearance activities and confirmation that tags were properly hung

and that equipment was appropriately configured to safely support the associated

work or testing

Installation and configuration of reactor coolant pressure, level, and temperature

instruments to provide accurate indication and instrument error accounting

Status and configuration of electrical systems and switchyard activities to ensure that

TSs were met

Monitoring of decay heat removal operations

Impact of outage work on the ability of the operators to operate the spent fuel pool

cooling system

Reactor water inventory controls, including flow paths, configurations, alternative

means for inventory additions, and controls to prevent inventory loss

Activities that could affect reactivity

Maintenance of secondary containment as required by TSs

Fatigue management

Refueling activities, including fuel handling and fuel receipt inspections

Tracking of startup prerequisites, walkdown of the drywell (primary containment) to

verify that debris had not been left which could block the emergency core cooling

system suction strainers, and startup and ascension to full power operation

Identification and resolution of problems related to refueling outage activities

b. Findings

No findings were identified.

14

.2

Unit 2 Forced Outage (1 sample)

a. Inspection Scope

The inspectors observed a Unit 2 forced outage following elevated unidentified reactor

coolant system (RCS) leakage, conducted December 13 to 15, 2015. The elevated

leakage was later identified to be a packing leak from the Unit 2 C inboard MSIV. The

inspectors reviewed Exelons development and implementation of the forced outage

schedule to verify that risk, industry experience, previous site-specific problems, and

defense-in-depth were considered. During the outage, the inspectors observed portions

of the shutdown and cooldown processes and monitored controls associated with the

following outage activities:

Configuration management, including maintenance of defense-in-depth,

commensurate with the forced outage plan for the key safety functions and

compliance with the applicable TSs when taking equipment OOS

Implementation of clearance activities and confirmation that tags were properly hung

and that equipment was appropriately configured to safely support the associated

work or testing

Monitoring of decay heat removal operations

Tracking of startup prerequisites, partial walkdown of the drywell to verify clearances

had been removed and debris had not been left around the C inboard MSIV which

could block the emergency core cooling system suction strainers, and startup and

ascension to full power operation

Identification and resolution of problems related to the forced outage activities

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22 - 5 samples)

a. Inspection Scope

The inspectors observed performance of STs and/or reviewed test data of selected risk

SSCs to assess whether test results satisfied TSs, the UFSAR, and PBAPS procedure

requirements. The inspectors verified that test acceptance criteria were clear, tests

demonstrated operational readiness and were consistent with design documentation,

test instrumentation had current calibrations and the range and accuracy for the

application, tests were performed as written, and applicable test prerequisites were

satisfied. Upon test completion, the inspectors considered whether the test results

supported that equipment was capable of performing the required safety functions.

The inspectors reviewed the following STs and routine tests:

Unit 3 B standby liquid control (SBLC) test on October 15, 2015

Unit 3 HPCI low pressure test on October 21, 2015

Unit 3 A MSIV closure test on October 26, 2015

Unit common, E-2 EDG monthly test on November 9, 2015

Unit 2 RCS unidentified leakage surveillance on December 7, 2015

15

b. Findings

Introduction. The inspectors identified a NCV of very low safety significance of

10 CFR Part 50, Appendix B, Criterion III, Design Control, for not ensuring that the

PBAPS EDG LO supply was designed to withstand the effects of natural phenomena.

Specifically, additional LO, evaluated by PBAPS to meet their EDG TS mission time of

seven days of continuous operation, was housed in a non-seismic Class 1 structure that

was not designed to withstand the effects of natural phenomena.

Description. On November 9, 2015, the inspectors reviewed IR 02583825, concerning

loss of LO inventory in the E-2 EDG LO storage tank during an E-2 EDG monthly ST.

The IR documented in its basis for operability that total LO inventory onsite was within

TS limits. In 1994, PBAPS converted from custom to ITS. During the ITS conversion,

the NRC requested PBAPS to evaluate the EDG LO consumption rate to determine if

inventory requirements met their intended design. In response to the request for

information, PBAPS evaluated, under evaluation A0784276, the oil consumption rate

to be 2.0 gallons per hour based both on vendor specifications and conservatism

recommended by the vendor since LO consumption is affected by the quality of the oil

used and engine wear. PBAPS identified that the EDGs required additional inventory to

meet their design requirements because of the consumption rate, capacity of the in-room

storage (i.e., LO tank, associated piping, and LO sump), and seven day continuous

operational design requirement.

TS 3.8.3 requires a LO inventory of 350 gallons per EDG to be operable. The TS bases

states that LO stored in the onsite warehouse can be credited towards achieving the

required inventory. PBAPS performs a monthly verification of EDG lubrication oil to

satisfy their TS requirement. The inspectors independently walked down the additional

inventory in PBAPS onsite warehouse and identified that the LO may become

unavailable during a natural phenomena event.

The EDGs are part of the standby safety power supply system. PBAPS UFSAR 8.5.2.4,

Safety Design Basis, states that, each diesel generator unit is housed in a seismic

Class I structure, and located such that the equipment is protected against other natural

phenomena such as flood, tornado, rain, ice, snow, and lightning. Furthermore, UFSAR

Section 8.5.4, Safety Evaluation, states, in part, that, diesel generator units are

capable of operating continuously for a period of seven days without any offsite

supplies, and that the units and all necessary auxiliary systems are housed in seismic

Class I structures and are protected against other natural phenomena. UFSAR 8.5.2.1

states that the standby alternating current power supply design conforms to the intent of

Proposed Institute of Electrical and Electronics Engineers (IEEE) Criteria for Class 1E

Electrical Systems for Nuclear Power Generating Stations, dated June, 1969. The

Proposed IEEE Criteria for Class 1E Electrical Systems for Nuclear Power Generating

Stations, dated June, 1969, Section 5.2.4, Standby Power Supply, states, in part, that

the standby power supply shall consist of all components from the stored energy to the

connection to the distribution systems supply breaker (e.g., generators and excitation

equipment; all auxiliary systems and appurtenances.) This standard was subsequently

approved as IEEE Standard 308-1971, IEEE Standard Criteria for Class 1E Electric

Systems for Nuclear Power Generating Stations, dated September 16, 1971, and which

contains an identical description of a standby power supply. The IEEE standard also

lists design basis events in Section 2 and in Table 1 to include the natural phenomena

(i.e., seismic, flood, tornado, etc.) to which the Class 1E Electric Systems must remain

functional under the conditions produced by the design basis events.

16

The inspectors questioned whether the LO stored in the warehouse was adequately

protected and would remain available for replenishment into the EDG system following

natural phenomena. The inspectors questioned how PBAPS ensured the integrity of the

LO barrels to maintain the LO free from containments that might be introduced during a

flood, and to prevent loss of the oil if the containers were damaged during a seismic

event or tornado. The inspectors also questioned the accessibility of the barrels, and

the feasibility of transporting the barrels from the warehouse to the EDG building during

natural phenomena.

The inspectors identified that since the warehouse was not a seismic Class I structure,

there is not reasonable assurance that the LO would be available for replenishment

following a seismic event. In addition, the inspectors reviewed PBAPS severe weather

and seismic event procedures and found no instructions or preparations to relocate the

required LO barrels in the event of natural phenomena. No additional design

documentation was identified approving the warehouse as an acceptable storage

location. As a result, PBAPS entered the issue into the CAP as IR 02603369 and took

immediate corrective actions to relocate the LO reserve inventory from the warehouse to

the 135 elevation of PBAPS radwaste building, which is listed in the UFSAR Appendix

C.1.2 as a seismic Class I structure. PBAPS specified a corrective action in IR

02603369 to evaluate a long term storage location and to enhance their severe weather

and natural phenomena procedures.

Analysis. PBAPS failure to ensure that the safety-related function of the EDG

lubrication system was not susceptible to natural phenomena was a performance

deficiency (PD). Specifically, barrels of LO for makeup to the EDGs credited towards the

TS 3.8.3 requirement of 350 gallons on site were stored in a warehouse that is not a

seismic Class I structure and would not be protected from natural phenomena specified

in PBAPS design basis. This PD was considered more than minor because it is

associated with the Protection Against External Factors Attribute of the Reactor Safety

Mitigating Systems cornerstone, and adversely affected the cornerstones objective of

ensuring reliability and capability of systems that respond to initiating events to prevent

undesirable consequences (i.e., core damage).

The inspectors evaluated the significance of this finding using IMC 0609 Appendix A,

The SDP for Findings at Power, Exhibit 2, Mitigating Systems Screening Questions.

The inspectors determined that this finding was of very low safety significance (Green)

because the finding is a design deficiency which did not result in an actual loss of

functionality of the EDGs.

This finding did not have a cross-cutting aspect because the most significant contributor

of the PD occurred during the 1994 conversion to ITS and, thus, was not reflective of

current plant performance. Specifically, PBAPS current engineering change request

(ECR) process would evaluate for natural phenomena considerations such as seismic,

tornado, flood, etc.

Enforcement. 10 CFR Part 50, Appendix B, Criterion III, Design Control, states, in part,

that measures shall be established to assure that applicable regulatory requirements

and the design basis as specified in the license are correctly translated into

specifications, drawings, procedures, and instructions, and that measures shall also be

established for the selection and review for suitability of application of materials, parts,

equipment, and processes that are essential to the safety-related functions of the SSCs.

Contrary to the above, PBAPS did not establish measures to review for suitability of

17

materials and processes that are essential to the safety-related functions of SSCs.

Specifically, PBAPS did not ensure the adequacy of PBAPS EDG LO supply design to

withstand the effects of natural phenomena. Because this finding is of very low safety

significance, and PBAPS has entered it into their CAP (IR 02603369), this violation is

being treated as an NCV, consistent with section 2.3.2a of the NRCs Enforcement

Policy. (NCV 05000277/278/2015004-01, Failure to Ensure Design Basis of EDG

Lubrication System)

Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation (71114.06 - 1 sample)

Emergency Preparedness (EP) Drill/Simulator Evaluation/Observation

a. Inspection Scope

The inspectors evaluated the shift manager\\emergency directors EP implementation

during a licensed operator annual requalification training scenario on November 9, 2015.

The inspectors observed emergency response operations in the simulator to determine

whether event classifications and notifications were performed in accordance with

approved procedures. The inspectors also attended the control room simulator drill

critique to compare inspector observations with those identified by PBAPS staff in order

to evaluate whether PBAPS staff was properly identifying emergency preparedness

weaknesses and entering them into the CAP.

b. Findings

No findings were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety (OS)

2RS1 Radiological Hazard Assessment and Exposure Controls (71124.01 - 1 sample)

a. Inspection Scope

During September 28 - October 2, 2015, the inspectors reviewed Exelons performance

in assessing and controlling radiological hazards in the workplace. The inspectors used

the requirements contained in 10 CFR 20, TSs, applicable Regulatory Guides (RGs),

and the procedures required by TSs as criteria for determining compliance.

Inspection Planning

The inspectors reviewed the performance indicators for the occupational exposure

cornerstone, radiation protection (RP) program audits, and reports of operational

occurrences in occupational radiation safety since the last inspection.

18

Radiological Hazard Assessment

The inspectors reviewed recent plant radiation surveys and any changes to plant

operations since the last inspection to identify any new radiological hazards for onsite

workers or members of the public.

Contamination and Radioactive Material Control

The inspectors observed the monitoring of potentially contaminated material leaving

the radiological control area and inspected the methods and radiation monitoring

instrumentation used for control, survey, and release of that material. The inspectors

selected several sealed sources from inventory records and assessed whether the

sources were accounted for and were tested for loose surface contamination. The

inspectors evaluated whether any recent transactions involving nationally tracked

sources were reported in accordance with requirements.

Radiological Hazards Control and Work Coverage

The inspectors evaluated in-plant radiological conditions and performed independent

radiation measurements during facility walk-downs and observation of radiological work

activities. The inspectors assessed whether posted surveys, radiation work permits

(RWPs), worker radiological briefings, the use of continuous air monitoring and

dosimetry monitoring were consistent with the present conditions. The inspectors

examined the control of highly activated or contaminated materials stored within the

spent fuel pools and the posting and physical controls for selected high radiation areas

(HRAs), locked high radiation areas (LHRAs) and very high radiation areas (VHRA) to

verify conformance with the occupational exposure control effectiveness performance

indicator.

Risk-Significant HRA and VHRA Controls

The inspectors reviewed the controls and procedures for HRAs, VHRAs, and radiological

transient areas in the plant.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with radiation monitoring and

exposure control were identified at an appropriate threshold and properly addressed in

the CAP.

b. Findings

No findings were identified.

2RS2 Occupational As Low As Reasonably Achievable (ALARA) Planning and Controls

(71124.02 - 1 sample)

a. Inspection Scope

During September 28 - October 2, 2015, the inspectors assessed Exelons performance

with respect to maintaining occupational individual and collective radiation exposures

19

ALARA. The inspectors used the requirements contained in 10 CFR 20, applicable

RGs, TSs, and procedures required by TSs as criteria for determining compliance.

Inspection Planning

The inspectors conducted a review of PBAPS collective dose history and trends;

ongoing and planned radiological work activities; radiological source term history and

trends; and ALARA dose estimating and tracking procedures.

Radiological Work Planning

The inspectors selected the following radiological work activities based on exposure

significance for review:

RWP PB-C-15-00823, Feed Water Heater Replacement (3AE003 & 3CE003)

RWP PB-C-15-822, Unit 3 High Pressure Turbine Disassembly, 1000 mrad,

Heavy Work, High Efficiency Particulate Air & Wet Surface

RWP PB-C-15-00510, Drywell Main Steam SRV Activities

RWP PB-C-1500513, Control Rod Drive Exchange, Effective Dose Equivalent

Monitoring Required

For each of these activities, the inspectors reviewed: ALARA work activity evaluations,

exposure estimates, and exposure reduction requirements.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with ALARA planning and

controls were identified at an appropriate threshold and properly addressed in the CAP.

b. Findings

No findings were identified.

2RS3 In-Plant Airborne Radioactivity Control and Mitigation (71124.03 - 1 sample)

a. Inspection Scope

During September 28 - October 2, 2015, the inspectors reviewed the control of in-plant

airborne radioactivity and the use of respiratory protection devices for radiological

protection. The inspectors used the requirements in 10 CFR 20, RG 8.15, RG 8.25,

NUREG/CR-0041, TS, and procedures required by TS as criteria for determining

compliance.

Inspection Planning

The inspectors reviewed the UFSAR to identify ventilation and radiation monitoring

systems associated with airborne radioactivity controls and respiratory protection

equipment staged for emergency use. The inspectors also reviewed respiratory

protection program procedures and current performance indicators for unintended

internal exposure incidents.

20

Use of Respiratory Protection Devices

The inspectors reviewed the adequacy of the licensees use of respiratory protection

devices in the plant to include applicable ALARA evaluations, respiratory protection

device certification, respiratory equipment storage, air quality testing records, and

individual qualification records.

Problem Identification and Resolution

The inspectors evaluated whether problems associated with the control and mitigation of

in-plant airborne radioactivity were identified at an appropriate threshold and addressed

by the licensees CAP.

b. Findings

No findings were identified.

2RS5 Radiation Monitoring Instrumentation (71124.05 - 1 sample)

a. Inspection Scope

During September 28 - October 2, 2015, the inspectors reviewed performance in

assuring the accuracy and operability of radiation monitoring instruments used to protect

occupational workers and for effluent monitoring and analysis. The inspectors used the

requirements in 10 CFR 20, 10 CFR 50, Appendix I; TSs; Offsite Dose Calculation

Manual (ODCM); RGs; applicable industry standards; and procedures required by TSs

as criteria for determining compliance.

Inspection Planning

The inspectors reviewed records of in-service survey instrumentation and procedures for

instrument source checks and calibrations.

Walkdowns and Observations

The inspectors conducted walk-downs of plant area radiation monitors, continuous

air monitors and radioactive gaseous and liquid effluent monitoring systems. The

inspectors reviewed the calibration and source check status of various portable radiation

survey instruments and contamination detection monitors for personnel and equipment.

Calibration and Testing Program

For the following radiation detection instrumentation, the inspectors reviewed the current

detector and electronic channel calibration, functional testing results and alarm set-

points: portal monitors; personnel contamination monitors; small article monitors;

portable survey instruments; area radiation monitors; electronic dosimetry; air samplers;

and continuous air monitors.

b. Findings

No findings were identified.

21

2RS6 Radioactive Gaseous and Liquid Effluent Treatment (71124.06 - 1 sample)

a. Inspection Scope

During September 28 - October 2, 2015, the inspectors reviewed the treatment,

monitoring, and control of radioactive gaseous and liquid effluents. The inspectors used

the requirements in 10 CFR 20, 10 CFR 50, Appendix I; TS; ODCM; applicable industry

standards; and procedures required by TSs as criteria for determining compliance.

Groundwater Protection Initiative (GPI) Implementation

The inspectors reviewed: groundwater monitoring results; changes to the GPI program

since the last inspection; anomalous results or missed groundwater samples; leakage or

spill events including entries made into the decommissioning files (10 CFR 50.75(g));

and Exelons evaluation of any positive groundwater sample results, including

appropriate stakeholder notifications and effluent reporting requirements.

b. Findings

No findings were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151 - 8 samples)

.1

Mitigating Systems Performance Index

a. Inspection Scope

The inspectors reviewed Exelons submittal for the Mitigating Systems Performance

Index (MSPI) for the period of October 1, 2014 through September 30, 2015.

Unit 2 and Unit 3 HPCI (MS07)

Unit 2 and Unit 3 RCIC (MS08)

Unit 2 and Unit 3 RHR (MS09)

Unit 2 and Unit 3 cooling water (MS10)

To determine the accuracy of the PI data reported during those periods, the inspectors

used definitions and guidance contained in Nuclear Energy Institute Document 99-02,

Regulatory Assessment PI Guideline, Revision 6. The inspectors also reviewed RCS

sample analysis and control room logs of daily measurements of RCS leakage, and

compared that information to the data reported by the PI.

b. Findings

No findings were identified.

22

4OA2 Problem Identification and Resolution (71152 - 3 samples)

.1

Routine Review of Problem Identification and Resolution Activities

a. Inspection Scope

As required by Inspection Procedure (IP) 71152, Problem Identification and Resolution,

the inspectors routinely reviewed issues during baseline inspection activities and plant

status reviews to verify that PBAPS entered issues into the CAP at an appropriate

threshold, gave adequate attention to timely corrective actions, and identified and

addressed adverse trends. In order to assist with the identification of repetitive

equipment failures and specific human performance issues for follow-up, the inspectors

performed a daily screening of items entered into the CAP and periodically attended

condition report screening meetings. The inspectors also confirmed, on a sampling

basis, that, as applicable, for identified defects and non-conformances, PBAPS

performed an evaluation in accordance with 10 CFR Part 21.

b. Findings

No findings were identified.

.2

Annual Sample: Trend of Leaks in the ESW and HPSW System Piping (1 sample)

a. Inspection Scope

The inspectors performed an in-depth review of Exelons apparent cause evaluation and

corrective actions associated with CR AR 01695675, ESW Pinhole Leak on Supply

Elbow to Unit 2 Ring Header. Specifically, a through-wall leak developed on an ESW

pipe fitting, which resulted in both subsystems of ESW being declared inoperable and an

entry into the action statement associated with TS 3.7.2. The inspectors also reviewed

leaks and wall thinning conditions identified in the HPSW system. Both the ESW and

HPSW systems use the Susquehanna River as a water source for providing cooling to

various safety-related plant components.

The inspectors assessed Exelons problem identification threshold, cause analyses,

extent of condition (EOC) reviews, compensatory actions, and the prioritization and

timeliness of Exelons corrective actions to determine whether Exelons staff were

appropriately identifying, characterizing, and correcting problems associated with the

leak and whether the planned or completed corrective actions were appropriate. The

inspectors compared the actions taken to Exelons CAP and the requirements of 10 CFR

50, Appendix B. The inspectors interviewed engineering personnel to discuss the

results of the cause evaluation and to assess the effectiveness of the implemented

corrective actions. The inspectors also conducted walkdowns of the accessible portions

of the ESW and HPSW systems to observe the general material conditions of the piping

and associated components.

b. Findings and Observations

No findings were identified.

23

Exelon staff determined the apparent cause of the emergency service water (ESW)

elbow leak was due to under deposit pitting corrosion and microbiologically influenced

corrosion in raw water (i.e., river water) piping, which was increased by flow effects in

this particular location. Specifically, deposits formed on the inside of the pipe from silt

and microbiological organisms associated with the untreated river water that led to

isolated pitting corrosion under the deposits and subsequently a pinhole leak. For the

ESW elbow leak, Exelon staff determined that there was one contributing cause due to

inadequate understanding of failure consequence and probability, which resulted in a

lower examination priority.

The inspectors concluded that Exelon staff conducted an appropriate review to identify

the likely causes of the piping leak. The inspectors also concluded that Exelon staff

identified the EOC, which included all safety-related raw water piping in Peach Bottom

Units 2 and 3. Immediate corrective actions included an evaluation of the component for

operability and structural integrity, scheduling for replacement of the leaking component,

and routine monitoring for any changes in leakage. The inspectors noted that Exelon

utilized ASME Code Case N-513-3 to evaluate the leak, which allows temporary

acceptance and operation of the component until replacement at the next RFO. Exelon

staff was required to submit a relief request to the NRC because Code Case N-513-3 is

limited to the evaluation of piping and does not include elbows, fittings, or other non-pipe

components. Exelon staff implemented further corrective actions, which included a

review of the raw water piping database to address the risk ranking factors and

consequences; revision of ER-AA-5400-1001, Raw Water Corrosion Program Guide,

to include additional guidance on risk ranking of piping with potential integrity threats;

evaluation of corrosion rates based on results of this leak and EOC inspections; and a

review of other elbows and fittings most susceptible to integrity concerns.

The inspectors reviewed Peach Bottoms raw water corrosion database, including a

sample of pipe locations currently being monitored for wall thickness, to verify that

Exelon staff were adequately tracking and prioritizing pipes for inspection and

replacement. The inspectors noted that the raw water corrosion engineer utilized a

supplemental database, which incorporated additional parameters for establishing

corrosion rates, estimating remaining life, and scheduling future inspections. The

inspectors also reviewed another Peach Bottom specific tool that used risk ranking for

large sections of system piping rather than individual pipe locations in order to prioritize

vulnerable sections of piping for future replacement.

In addition, the inspectors reviewed currently ongoing and planned raw water piping

projects to verify that Exelon staff were proactively mitigating piping integrity issues.

One recent project involved the replacement of high risk-based piping at the ESW

pumps discharge. While there were no chemistry control corrective actions identified in

the apparent cause evaluation, the inspectors noted that there is a planned project in the

review process to evaluate potential combinations of chemistry controls and cleaning for

internal pipe corrosion. The inspectors determined Exelons overall response to the

ESW elbow leak as well as other related raw water issues was commensurate with the

safety significance, was timely, and included appropriate compensatory actions. The

inspectors concluded that completed and planned actions were reasonable to correct the

problem and help prevent reoccurrence.

24

.3

Annual Sample: Review of Unit 2 Torus Coating Defects (1 sample)

a. Inspection Scope

The inspectors reviewed corrective actions completed by Exelon staff as a consequence

of CR 02413128, Coating Defects and Pinpoint Rust in Torus Belly Band Area, and CR

02407173, Pit with Depth of 126 mils. The inspectors reviewed the results of Exelons

report to identify, prioritize and resolve the causes of the coating defects, rust, and

pitting. The inspectors also reviewed results of torus examinations on a sampling basis

for the previous PBAPS Unit 2 RFOs back to 2006, and Unit 3 RFOs back to 2007.

The inspectors determined if the completion of corrective actions was in a timely manner

commensurate with the safety significance of the issue. The inspectors considered if

any delays in implementation were justified based on the safety significance of the issue.

The inspectors considered if any permanent corrective actions required significant time

to implement and if interim corrective actions and/or compensatory actions were

identified and implemented to minimize the problem and/or mitigate its effects until the

permanent action could be implemented.

The inspectors reviewed the actions taken to determine if the actions resulted in the

correction of the identified problem. In the case of this condition, the inspectors

determined if the corrective action taken would preclude repetition. Finally the

inspectors reviewed operating experience to determine if it was adequately evaluated

for applicability, and applicable lessons learned were communicated to appropriate

organizations and implemented.

b. Findings and Observations

No findings were identified.

The corrective action of the coating defects and pinpoint rust in the torus belly band

area, was to continue to monitor this area for further degradation. Exelon staff took into

account operability, consideration of EOC and cause, generic implications, common

cause, and previous occurrences. This corrective action was reviewed by the inspectors

to determine if the classification and prioritization of the problems resolution was

commensurate with the safety significance.

The corrective action for the pit with a depth of 126 mils was to determine if the pit

impacted operability and to repair and recoat the area. Exelon staff took into account

the EOC by reviewing prior inspection reports for the area associated with the pit to

determine if other pits, in the immediate area which had been repaired previously, could

impact the integrity of the newly discovered pit. Exelon staff took into consideration

generic implications, common cause, and previous occurrences. This corrective action

was reviewed by the inspectors to determine if the classification and prioritization of the

problems resolution was commensurate with the safety significance.

The inspectors interviewed station personnel involved in developing the monitoring and

repair plans. The derived information was compared with the corrective actions

identification of contributing causes of the problem. The inspectors ascertained if the

documented information was reported to appropriate levels of management. The

25

inspectors reviewed the corrective action to determine if the corrective action was

appropriately focused to correct the problem (and to address the root and contributing

causes for significant conditions adverse to quality).

The inspectors review determined Exelon staff established a defined threshold to assure

that no pit would threaten the torus minimum wall thickness prior to the torus recoat

activity. The threshold was sufficient to ensure that the torus pressure boundary

remained acceptable. The inspectors determined the threshold included a corrosion

allowance for all uncoated pits based on actual corrosion data and the planned recoat

schedule. The inspectors determined that pits with depths exceeding the defined

threshold were evaluated by Exelon engineering staff and were coated to assure no

further degradation.

The inspectors determined the actions of monitoring, analysis, and recoating resulted in

the correction of the identified problem. The inspectors determined the actions

maintained the safety barrier integrity by assuring the torus wall thickness was above the

design minimum requirement.

.4

Semi-Annual Trend Review (1 sample)

a. Inspection Scope

The inspectors performed a semi-annual review of site issues to identify trends that

might indicate the existence of more significant safety concerns. As part of this review,

the inspectors included repetitive or closely-related issues documented by PBAPS in

trend reports, site PIs, priority work lists, system health reports, MR assessments, and

maintenance or CAP backlogs. The inspectors also reviewed PBAPS CAP database

for the third and fourth quarters of 2015 to assess IRs written in various subject areas

(equipment problems, human performance issues, etc.), as well as individual issues

identified during the NRCs daily CR review (Section 4OA2.1). The inspectors reviewed

the PBAPS quarterly trend report for the third quarter of 2015, conducted under PI-AA-

125-1005, Coding and Analysis Manual, Revision 0, to verify that PBAPS personnel

were appropriately evaluating and trending adverse conditions in accordance with

applicable procedures.

b. Findings and Observations

No findings were identified.

The inspectors evaluated a sample of CRs generated over the course of the past two

quarters by departments that provide input to the quarterly trend reports. The inspectors

determined that, in most cases, the issues were appropriately evaluated by PBAPS staff

for potential trends and resolved within the scope of the CAP. The inspectors did

identify repeated occurrences regarding a lack of awareness in the travel path of check

valve swing arms in safety-related systems which did or could have impacted system

operability. The inspectors identified three occurrences where PBAPS obstructed the

travel path of check valve swing arms identified in IRs 1680741, IR 2519751, and IR

2559874. PBAPS initiated IR 2574611 to document the inspectors concern and

evaluate how to increase awareness of the travel path of safety-related check valve

swing arms.

26

The inspectors also noted and discussed with PBAPS staff ongoing minor adverse

trends in rigor and attention to detail in CAP products, including apparent cause

evaluations and work group evaluations, and in configuration control with tasks

performed by PBAPS maintenance department. However, the inspectors determined

that there were no adverse safety consequences as a result of these low level trends.

Based on the overall results of the semi-annual trend review, the inspectors determined

that PBAPS was appropriately identifying and entering issues into the CAP, adequately

evaluating the identified issues, and properly identifying adverse trends before they

became more safety significant operability problems.

4OA3 Follow-Up of Events and Notices of Enforcement Discretion (71153 - 1 sample)

(Closed) Licensee Event Report (LER) 05000/277-2-15-001: Condition Prohibited by

TS Due to Insufficient Remote Shutdown System Surveillance Testing

The NRC determined on September 4, 2015, that insufficient surveillance requirement (SR) 3.3.3.2.1 testing was being performed for certain functions from the remote

shutdown system (RSS) panel. Subsequently, during surveillance testing performed on

September 16, 2015, operations personnel identified that the RCIC system steam

admission valve (MO-2-13-131) would not open when operated from the RSS panel.

Prompt troubleshooting performed on September 16, 2015, identified that a wire within

the RSS panel associated with the logic for the MO-2-13-131 valve was not connected.

This condition did not impact the normal operation of the MO-2-13-131 valve from the

MCR, nor did it impact the automatic function of the MO-2-13-131 valve for licensed

events. Only the manual open function of the valve from the RSS panel (located outside

of the control room) was affected. The disconnected wire was re-landed and the MO-2-

13-131 was verified to operate properly from the RSS panel. The cause of the event

was previous insufficient RSS panel testing that did not detect this disconnected wire.

Surveillance test procedures of the RSS panel functions have been upgraded. A Green

NCV of TS 5.4.1a was identified and documented in the 2015003 inspection report (NCV

05000277/278/2015003-01, Incomplete Testing of Components from the Remote

Shutdown Panel). This LER is closed.

4OA5 Other Activities

Extended Power Uprate (EPU) Closure and Summary (71004)

a. Inspection Scope

On August 25, 2014, the NRC approved PBAPS License Amendments Nos. 293 and

296 for an approximately 12.4-percent EPU at Units 2 and 3 and issued the associated

safety evaluation (ADAMS package ML122860201). The inspectors have observed and

reviewed selected activities throughout the phased EPU implementation on both units.

The inspectors have determined, based on a sample review of these activities and

comparison of records and tests with the current licensing documents, that Exelons

commitments have been met regarding the PBAPS Unit 2 and Unit 3 EPU and that

Exelon has fully implemented the EPUs within its approved implementation timelines.

27

As required by IP 71004, Power Uprate, all inspection sample requirements for the

power uprate on Unit 2 and Unit 3 have been verified completed and recorded,

consistent with the inspection plan. This entry provides a summary of all inspection

samples associated with implementation of and as required by IP 71004.

Inspection Sample

Inspection Procedure (IP)

Inspection Report

Operator Simulator

Scenario

71111.11, 71004

2014004

Operator Simulator

Scenario

71111.11, 71004

2014005

EC/FAC

71004

2014005

Integrated Plant

Evolutions

71004

2014005

Major Plant Tests

71111.20, 71004

2014005

CST Standpipe

Modification

71111.17, 71004

2015002

Unit 2 HPSW Cross-tie

Modification

71111.17, 71004

2015002

Unit 3 A RHR Cross-tie

Modification PMT

71111.19, 71004

2015004

Unit 2 B CS Suction

MOV

71111.21, 71004

2015002

Unit 3 SBLC IST

71111.22, 71004

2015004

b. Findings

No findings were identified.

4OA6 Meetings, Including Exit

Quarterly Resident Exit Meeting Summary

On January 15, 2016, the inspectors presented the inspection results to Mr. Pat Navin,

Peach Bottom Plant Manager, and other members of the PBAPS staff. The inspectors

verified that no proprietary information was retained by the inspectors or documented in

this report.

ATTACHMENT: SUPPLEMENTARY INFORMATION

A-1

Attachment

SUPPLEMENTARY INFORMATION

KEY POINTS OF CONTACT

Exelon Generation Company Personnel

M. Massaro, Site Vice President

P. Navin, Plant Manager

J. Armstrong, Regulatory Assurance Manager

J. Boil, EPU RHR Project Manager

G. Cilluffo, Raw Water Corrosion Engineer

D. Dullum, Regulatory Assurance Engineer

J. Hawkins, Exelon NDE Level III

B. Holmes, Radiation Protection Manager

H. McCroy, Radiation Protection Technical Support Manager

B. Rufo, ISI Program Owner

NRC PERSONNEL

B. Smith, (Acting) Senior Resident Inspector

L. Micewski, (Acting) Senior Resident Inspector

B. Reyes, (Acting) Senior Resident Inspector

J. Patel, (Acting) Resident Inspector

S. Barber, Senior Project Engineer

N. Floyd, Reactor Inspector

C. Graves, Health Physicist

C. Highley, Project Engineer

D. Kern, Senior Reactor Inspector

M. Modes, Reactor Inspector

D. Orr, Senior Reactor Inspector

A. Turilin, Project Engineer

LIST OF ITEMS OPENED, CLOSED, DISCUSSED, AND UPDATED

Opened/Closed

05000277/278/2015004-01 NCV

Failure to Ensure Design Basis of Emergency

Diesel Generator Lubrication System

(Section 1R22)

Closed

05000277/2-15-001

LER

Condition Prohibited by TS Due to Insufficient

Remote Shutdown System Surveillance Testing

(Section 4OA3)

A-2

LIST OF DOCUMENTS REVIEWED

Section 1R01: Adverse Weather

Procedures

MA-PB-1003, Winter Readiness and Storm Response Guidelines for the Peach Bottom Facility,

Revision 11

OP-AA-108-111-1001, Severe Weather and Natural Disaster Guidelines, Revision 13

OP-PB-108-111-1001, Preparation for Severe Weather, Revision 13

RT-I-066-200-2, Heat Trace System Testing, Revision 11

RT-O-040-620-2, Outbuilding HVAC and Outer Screen Inspection for Winter Operation,

Revision 22

RT-O-040-630-2, Winterizing Procedure, Revision 14

WC-AA-107, Seasonal Readiness, Revision 16

IRs

01610850

02481268

Miscellaneous

Memo from M. Massaro to T. Dougherty, Certification of 2015-2016 PBAPS Winter Readiness,

dated October 29, 2015

Section 1R04: Equipment Alignment

Procedures

ARC-325 30C203B D-1, B RHR Pump Auto Start

SO 10.1.E-3, RHR System Torus Cooling Using the RHR Loop Cross-Tie

SO 13.1.B-3 COL, RCIC System Control Board Lineup, Revision 3

SI3M-2-SRV-XXMM, Instrument Check of SRV Position Indicators, Revision 8

SI3T-2-SRV-XXF2, Channel Functional Check of MSRV MSSV Thermocouples, Revision 2

Section 1R05: Fire Protection

Procedures

CC-AA-201, Plant Barrier Control Program, Revision 2

CC-AA-209, Fire Protection Program Configuration Change Review, Revision 5

CC-AA-211, Fire Protection Program, Revision 6

LS-AA-128, Regulatory Review of Proposed Changes to the Approved Fire Protection Program,

Revision 2

OP-AA-201-009, Control of Transient Combustible Material, Revision 17

PF-12C, Unit 3 Recirculation Pump MG Set Room Pre-Fire Strategy Plan, Revision 7

PF-117, Unit 3 Turbine Building, Emergency Battery Switchgear Rooms, Elevation 135-0,

Revision 10

PF-78H, Turbine Building Common, Cable Spreading and Computer Rooms - Elevation 150-0,

Revision 9

RT-O-57A-745-1, Balance of Plant and Miscellaneous Battery Monthly Check, Revision 16

RT-O-100-505-2, Emergency Operating Procedure Tool Inventory, Revision 39

A-3

Drawings

Drawing No. E-1313, Sheet 47D, Lighting Symbol, Notes & Details, Revision 1

Drawing No. 6260-E-1069, Sheet 1, Lighting, Communications & Power Layout - Control Room,

Revision 18

ARs

AR 01554568

AR 01646155

AR 02581778

AR 951114951114

AR 2022234

AR 2580969

Miscellaneous

MR System Basis Document for Emergency DC Lighting, System 57E

Section 1R07: Heat Sink Performance

Procedures

ER-AA-340-1002, Service Water HX Inspection Guide, Revision 6

CRs

01619316

Miscellaneous

2nd Trimester, 2015 PBAPS GL 89-13 Program Health Report

PM-0589, RHR HX Performance Evaluation, Revision 5

RHR System Periodic Review Meeting Notes dated March 27, 2015

RT-O-010-660-2, RHR HX Performance Test, Performed February 12, 2015

RT-X-010-661-2, RHR HX Performance Calculation Test, Performed March 25, 2015

WOs

R0963795

Section 1R08: In-service Inspection

Procedures

100-RT-001, Radiographic Examination in Accordance with ASME Section V, Article 2,

Revision 8

386HA480, GE Hitachi Nuclear Energy Written Practice for Certification of Nondestructive Test

Personnel, Revision 26

GEH-PDI-UT-5, PDI Generic Procedure for Straight Beam Ultrasonic Examination of Bolts and

Studs, Revision 6.1

GEH-UT-300, Procedure for Manual Examination of Reactor Vessel Assembly Welds,

Revision 12

GEH-UT-311, Procedure for Manual Examination of Nozzle Inner Radii and Bore, Revision 19

MA-PB-793-001, Visual Examination of Containment Vessels and Internals, Revision 2

ST-N-080-900-3, Visual Examinations of Drywell and Torus Surfaces, Revision 4

Drawings

6280-ISI-401, Sheet 4, ASME Section XI ISI Boundaries Drywell I.D. Roll-out and Penetrations,

Revision 0

A-4

CRs

01559490

02557950

02558014

02558524

WOs

C0255830

C0255936

C0255941

R1208385

Miscellaneous

ASME Repair/Replacement Plan for RHR Cross-tie Piping and Support Welds, dated

April 29, 2015

Completed Procedure ST-N-080-900-3 with Attached ASME IWE/IWL Visual Exam NDE

Reports, dated October 15, 2013

ECR 11-00376, RHR Cross-Tie Modification for EPU - Unit 3 A/C Trains, Revision 6

Focused Area Self-Assessment for ISI Program, dated September 3, 2015

GE Customer Notification Form 004, dated September 26, 2015

GE Customer Notification Form 006, dated September 28, 2015

IHI Reactor Vessel NDE Project Plan, Revision 0

Multiple VT Data Reports for ASME IWE/IWL Drywell Interior and Exterior from Procedure

MA-PB-793-001, dated October 2015

Owner's Activity Report for the 19th RFO for Unit 3, dated January 21, 2014

Owner's Activity Report for the 20th RFO for Unit 2, dated March 3, 2015

Peach Bottom ISI Program Plan for the 4th 10-Year Inspection Interval, Revision 4

Report 003600, UT Data Sheet for N4E Feedwater Nozzle-to-Vessel Weld, dated

September 27, 2015

Report 003650, UT Data Sheet for N4E Feedwater Nozzle Bore, dated September 28, 2015

Report 006350, UT Data Sheet for N4E Feedwater Nozzle Inner Radius, dated September 28,

2015

Report 010705, UT Data Sheet for RPV Studs 47-92, dated September 23, 2015

RPV Stud Qualification for NDE Personnel, dated September 24, 2015

RT Data Sheet for Weld 10-2DC20-29, dated September 30, 2015

RT Data Sheet for Weld 10-2XC020-11, dated October 2, 2015

RT Data Sheet for Weld 10-2XC020-12, dated October 2, 2015

Weld Information Data Sheet for 10-2DC20-29, dated September 28, 2015

Weld Information Data Sheet for 10-2XC020-11 and -12, dated September 28, 2015

Weld Traveler 212824-TR-308 for 10-2DC20-29, dated September 28, 2015

WPS-01-01-TS-200, Weld Procedure Specification for Manual GTAW/SMAW of P1 Metals,

Revision 9

Section 1R11: Licensed Operator Requalification Program

Procedures

OP-AA-101-115, Senior Management of the Operating Crews, Revision 4

Miscellaneous

PSEG-0235R Scenario 1, Group 1/ATWS

PSEG-0235R Scenario 2, Turbine Trip/ATWS

Peach Bottom Unit 3 BOC Startup Checklists

Peach Bottom Unit 2 BOC Startup Checklists

A-5

Section 1R12: Maintenance Effectiveness

Procedures

ER-AA-200-1001, Equipment Classification, Revision 1

ARs

02459304

CRs

02455787

02459304

02459304-05

Miscellaneous

PI-AA-125-1003, Apparent Cause Investigation Report (Equipment), Revision 2

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

Procedures

OP-AA-108-117, Protected Equipment Program, Attachment 1 - Protected Equipment Work

Approval Form September 25, 2015, B and D CS, Revision 4

Miscellaneous

EGM 11-003, Revision 2, Memo to William Dean from Roy Zimmerman, dated

December 13, 2013

WOs

C0254584

Miscellaneous

Paragon Risk Profiles, October 1, 2015

Section 1R15: Operability Evaluations

Procedures

OP-AA-102-103, OWA Program, Revision 4

ST-O-011-405-3, Standby Liquid Control B Loop Injection Test, Revision 12

OP-AA-102-103, OWA Program, Revision 4

AR

A1985864

02574110

CRs

02561427

02563769

02574110

WOs

C0256242

A-6

Drawings

LR-M-358, Standby Liquid Control System, Sheet 1, Revision 0

P&I Diagram, ESW and HPSW Systems

Miscellaneous

OWA Board Meeting Minutes, dated March 19, 2014

OWA Board Meeting Minutes, dated April 29, 2014

OWA Board Meeting Minutes, dated June 17, 2014

OWA Board Meeting Minutes, dated October 1, 2014

OWA Board Meeting Minutes, dated December 30, 2014

OWA Board Meeting Minutes, dated March 26, 2015

OWA Board Meeting Minutes, dated June 26, 2015

Section 1R18: Plant Modifications

Procedures

CC-AA-102, Design Input and Configuration Change Impact Screening, Revision 28

CC-AA-103, Configuration Change Control for Permanent Physical Plant Changes, Revision 27

CC-AA-104, Document Change Requests, Revision 16

CRs

02577302

02577693

02579116

02581643

02581644

02581240

02582201

Modifications

ECR: PB 13-00338, Unit 3 Recirculation MG Replacement - Outage Phase, Revisions 0, 1, 3,

and 4

ECR: PB 13-00340, Unit 3 Reactor Recirculation MG Set Decommissioning, Revision 0

ECR: PB 13-00341, Unit 3 Replacement of Reactor Recirculation System MGs with ASDs

(Pre-Outage P3R20 Work Scope), Revision 0, 1, 2, and 3

ECR: PB 14-00356, ASD Structure, Revisions 0, 1, and 2

Training Documents

N-PB-ENG-CT-1502B, Recirculation Adjustable Speed Drives (ASD), Revision 0

PLORT-1409C, Licensed Operator Training for ASD Modification to Unit 3 Reactor Recirculation

System, Revision 0

PSEG-0234R, ASD Operations Training Guide, Revision 0

Siemens Water-Cooled III, High Availability Variable Frequency Drive, Revision 0

Miscellaneous

MAT PB 13-00338-1-3, Unit 3 Adjustable Speed Drive (ASD) Uncoupled Recirculation Pump

Motor Modification Acceptance Test, Revision 0

MAT PB 13-00338-2-3, Unit 3 ASD Coupled Recirculation Pump Motor Modification Acceptance

Test dated October 20, 2015

MAT PB 13-00338-3-3, Unit 3 ASD Power Ascension Modification Acceptance Test, Revision 0

MAT PB 13-00341-1-3, Unit 3 ASD Cooling Water Modification Acceptance Test dated

September 24, 2015

A-7

Section 1R19: Post-Maintenance Testing

Procedures

ST/LLRT 30.01A.02, MSIV LLRT, Revision 14

ST/LLRT 30.14.01, LLRT CS A Loop, Revision 14

ST/LLRT 30.23.08, LLRT HPCI Vacuum Relief Valves, Revision 6

RT-O-013-240-3, RCIC Overspeed Trip Test Using Aux Steam, Revision 1

ST-O-032-301-3, HPSW Pump, Valve and Flow Functional and Inservice Test, Revision 31

IC-C-11-2009, Field Testing of Power Transformers, Revision 0

MA-AA-716-004, Complex Troubleshooting Data Sheet A, Revision 12

MA-AA-716-004, Support/Refute Method, Revision 13

MA-AA-716-012, PMT, Revision 20

ARs

C0256126

R1271865

R1122613

A1930510

A1546929

A1484162

A1049047

A1678925

A1600928

A1891126

A1975865

01171049

02600713

CRs

02561049

02561375

02570399

02587931

025888888

025888889

02589442

02589443

02590036

02599822

WOs

R1128367

R1128369

R1274711

R1018560

R1018560

R1018560

R0901395 C0172705

R1056916

R1249350

Miscellaneous

3 B Feedwater Testing and Maintenance Schedule

RHR P3R20 Planning Punchlist, Revision 8, dated March 10, 2015

Section 1R20: Refueling Outage

Procedures

OP-AA-108-108, Attachment 1, Engineering Department Start-Up Checklist, Revision 18

OP-AA-108-108, Attachment 9, Emergency Exceptions Checklist, Revision 18

ARs

A1930510

A1546929

A1484162

A1049047

A1678925

A1600928

A1891126

A1975865

02600713

01171049

CRs

02494904

02561427

02600168

02599822

WOs

R1274711

R1018560

R1018560

R1018560

C0172705

R1056916

R1249350

R0901395

C0172705

R1056916

R1249350

Section 1R22: Surveillance Testing

Procedures

A-8

EP-AA-1007, Addendum 3, Revision 0

MA-AA-723-301, Periodic Inspection of Limitorque Model SMB/SB/SBD-000 Through 5 Motor

Operated Valves, Revision 10

MA-AA-723-301, Periodic Inspection of Limitorque Model SMB/SB/SBD-000 Through 5 Motor

Operated Valves, Revision 11

PI-AA-120, Issue Identification and Screening Process, Revision 3

RRC 94.1-2, Reactor Operator Scram Actions

RRC 94.2-2, Plant Reactor Operator Scram Actions, Revision 3

SE-13.1-2, RCIC Manual Operations on Loss of 125/250 VDC Bus 2DA-W-A, Revision 0

SE-1 Bases, SE-1 Plant Shutdown from the Remote Shutdown Panel - Bases, Revision 22

SE-1 Procedure, SE-1 Plant Shutdown From the Remote Shutdown Panel - Procedure,

Revision 22

SO 13.7.A-2, Recovery From RCIC System Isolation or Turbine Trip, Revision 14

ST-O-033-750-2, ESW Pump Remote Shutdown Panel Test, Revision 0

ST-O-052-412-2, E-2 Diesel Generator Fast Start and Full Load Test, Revision 23

ST-O-052-202-2, E-2 Diesel Generator Slow Start and Full Load Test, Revision 21

ST-O-003-901-2, CRD Pump Remote Shutdown Panel Test, Revision 0

ST-O-003-901-3, CRD Pump Remote Shutdown Panel Test, Revision 0

ST-O-011-405-3, Standby Liquid Control System B Loop Injection Test, Revision 12

ST-O-013-201-2, RCIC Alternative Control Panel Test, and Remote Shutdown Panel Test,

Revision 5

ST-O-013-201-2, RCIC Alternative Control Panel Test, and Remote Shutdown Panel Test,

Revision 6

ST-O-013-201-3, RCIC Alternative Control Panel Test, and Remote Shutdown Panel Test,

Revision 5

ST-O-013-301-2, RCIC Pump, Valve, Flow and Unit Cooler Functional and In-service Test,

Revision 45

ST-O-013-750-3, Emergency Shutdown Control Panel Test, Revision 7

ST-O-013-750-2, Emergency Shutdown Control Panel Test, Revision 8

ST-O-013-750-2, Emergency Shutdown Control Panel Test, Revision 9

ST-O-023-200-3, HPCI Flow Rate at 175 PSIG Steam Pressure, Revision 17

ARs

A1978308

02414219

A2012485

A2015148

CRs

02012485

02413679

02414219

02526507

025500445

02551342

02551348

02556042

02556608

02556651

02556526

02555841

02558858

02556564

02575136

Drawings

M-1-S-42, Electrical Schematic Diagram RCIC System, Revision 75

SE-10, Alternative Shutdown, Revision 20

6280-M-365

6280-M-366

Miscellaneous

Appendix A Surveillances

Limitorque Technical Update 14-01, Issue Date: August 25, 2014

Remote Shutdown System 3.3.3.2, PBAPS Unit 3, Amendment No. 281

Remote Shutdown System B 3.3.3.2, PBAPS Unit 2, Revision No. 0

A-9

Remote Shutdown System 3.3.3.2, General Electric BWR/4 STS, 3.3.3.2-1, Revision 4.0

Position Paper for Justifying Compliance with LCO 3.3.3.2, Remote Shutdown System

Surveillance Requirement SR 3.3.3.2.1 (IR 2526507)

Unit 2 Limiting Conditions for Operation, Surveillance Requirements, Amendment No. 184

TSCR 93-16, PBAPS Current TSs Comparison Document

TS 3.6.1

TS 3.6.1.3

TS 3.8.1

STI-28, Shutdown From Outside the Control Room

ARC-0AC097 B-6, Revision 6

Section 1EP6: Drill Evaluation

Procedures

OP-AA-101-115, Senior Management of the Operating Crews, Revision 4

Miscellaneous

PSEG-0235R Scenario 1, Group 1/ATWS

PSEG-0235R Scenario 2, Turbine Trip/ATWS

Section 2RS1: Access Control to Radiologically Significant Areas

Procedures

RP-AA-19, HRA Program Description, Revision 2

RP-AA-100, Conduct of Radiation Protection Operations, Revision 0

RP-AA-111, Advanced Radiation Worker (ARW), Revision 2

RP-AA-460, Controls for High and LHR Areas, Revision 26

RP-AA-460-002, Additional High Radiation Exposure Control, Revision 2

RP-AA-1008, Unescorted Access to and Conduct in Radiologically Controlled Areas, Revision 4

Documents

Unit 3 TSs

Unit 3 UFSAR

DW Survey All Levels Weeks of September 21, 2015 & September 28, 2015

Section 2RS2: Occupational ALARA Planning and Controls

Procedures

RP-AA-401, Operational ALARA Planning and Controls, Revision 19

RP-AA-401-1002, Radiological Risk Management, Revision 7

RP-AA-403, Administration of the Radiation Work Permit Program, Revision 6

Documents

RWP PB-C-15-00823, Feedwater Heater Replacement (3AE003 & 3CE003)

Wet Surface

RWP PB-C-15-00510, DW Main Steam SRV Activities

RWP PB-C-1500513, CRD Exchange, EDE Monitoring Required

A-10

Section 2RS3: In-plant Airborne Radioactivity Control and Mitigation

Procedures

RP-AA-440, Respiratory Protection Program, Revision 10

RP-AA-441, Evaluation and Selection Process for Radiological Respirator Use, Revision 5

RP-AA-301, Radiological Air Sampling Program, Revision 8

RP-AA-825-1001, Inspection of Respiratory Protection Equipment, Revision 5

RP-AA-825-1020, Operation and Use of Air Line Supplied Respirators, Revision 0

RP-PB-825-1011, Inspection and Use of the Muroroa V4 F1R Air Supplied Suit, Revision 2

Documents

NRC Approval Letter to Use Non-NIOSH approved Delta Suit, January 31, 2005

Breathing Zone Air Sample 15-07931 September 23, 2015

Breathing Zone Air Sample 15-08511 September 26, 2015

Work Area Air Sample for Valve MO-3-14-12A Breach September 27, 2015

Section 2RS5: Radiation Monitoring Instrumentation

Procedures

RP-AA-700-1501, Operation and Calibration of the Model SAM-9/11 Small Articles Monitor,

Revision 1

RP-AA-700-1214, Operation and Calibration of the PCM-1B Personnel Monitor, Revision 1

RP-AA-700-1240, Operation and Calibration of the Canberra ARGOS-5 Personnel

Contamination Monitor, Revision 2

RP-AA-700-1239, Operation and Calibration of the SAM-12 Small Articles Monitor, Revision 1

RP-AA-700-1235, Operation and Calibration of the PM-12 Portal Monitor, Revision 1

Section 2RS6: Radioactive Gaseous and Liquid Effluent Treatment

Procedures

CY-AA-130-205-F-02, Tritium, Gross Alpha, and Gross Beta Sample Preparation for

Scintillation Counting, Revision 2

CY-AA-170-000, Radioactive Effluent and Environmental Monitoring Programs, Revision 6

CY-AA-170-1000, Radiological Environmental Monitoring Program and Meteorological Program

Implementation, Revision 8

ODCM, Revision 15

Section 4OA1: Performance Indicator Verification

Procedures

ER-AA-2008, MSPI Monitoring and Margin Evaluation, Revision 4

LS-AA-2200, MSPI Data Acquisition and Reporting, Revision 5

LS-AA-2200, Reactor Core Isolation Data Sheets, October 2014 - September 2015, Revision 5,

Attachment 3

LS-AA-2200, High Pressure Injection Data Sheets, October 2014 - September 2015,

Revision 5, Attachment 2

CRs

02426670

02412767

02413412

02412748

02411606

02409746

A-11

Section 4OA2: Problem Identification and Resolution

Procedures

ER-AA-5400, Underground (Buried) Piping and Raw Water Corrosion Program (UPRWCP)

Guide, Revision 8

ER-AA-5400-1001, Raw Water Corrosion Program Guide, Revision 8

PI-AA-125, CAP Procedure, Revision 2

PI-AA-125-1005, Coding and Analysis Manual, Revision 0

Drawings

6280-M-315, Sheet 1, P&ID ESW and HPSW Systems, Revision 83

6280-M-315, Sheet 4, P&ID ESW and HPSW Systems, Revision 56

CRs

01411997

01680741

01695675

02407173

02411498

02413128

02427541

02489386

02494904

02519751

02520612

02559874

02568856

02574611

Miscellaneous

Apparent Cause Investigation Report titled "ESW Pinhole Leak on Supply Elbow to Unit 2 Ring

Header" (AR 01695675), dated October 15, 2014

Apparent Cause Investigation Report Titled, "HPSW Pipe Below Minimum Required Thickness"

(AR 01411997), dated September 27, 2012

PVP2014-28781, Piping Corrosion Rate & Remaining Life Basis: Commercializing

Conservatism in First Time Inspections, Revision 0

Third and Fourth Quarter 2015 Station Trend Reports

Technical Evaluation CC-AA-309-101, 2407173-2, Pit evaluation

Section 4OA3: Follow-up of Events and Notices of Enforcement Discretion

Miscellaneous

LER 05000/277-2-15-001: Condition Prohibited by TS Due to Insufficient Remote Shutdown

System ST

A-12

LIST OF ACRONYMS

ADAMS

Agencywide Documents Access and Management System

ALARA

as low as reasonably achievable

ASD

adjustable speed drive

ASME

American Society of Mechanical Engineers

CAP

corrective action program

CFR

Code of Federal Regulations

CR

condition report

CS

core spray

ECR

engineering change request

ECT

emergency cooling tower

EDG

emergency diesel generator

EP

emergency preparedness

EPU

extended power uprate

ESW

emergency service water

GPI

groundwater protection initiative

HPCI

high pressure coolant injection

HPSW

high pressure service water

HRA

high radiation area

HX

heat exchanger

IEEE

Institute of Electrical and Electronics Engineer

IMC

inspection manual chapter

IP

inspection procedure

IR

issue report

ISI

in-service inspection

ITS

improve technical specifications

LER

licensee event report

LHRA

locked high radiation area

LLRT

local leak rate test

LO

lubrication oil

MG

motor generator

MR

maintenance rule

MSIV

main steam isolation valve

MSPI

mitigating system performance index

NCV

non-cited violation

NDE

non-destructive examination

NRC

Nuclear Regulatory Commission

ODs

operability determinations

ODCM

offsite dose calculation manual

OOS

out of service

OWAs

operator workarounds

PARS

publicly available records

PBAPS

Peach Bottom Atomic Power Station

PD

performance deficiency

PI

performance indicator

PMT

post-maintenance testing

RFO

Refueling Outage

RCIC

reactor core isolation cooling

A-13

RCS

reactor coolant system

RG

Regulatory Guide

RHR

residual heat removal

RP

radiation protection

RPM

radiation protection manager

RSS

remote shutdown system

RT

radiographic testing

RTP

rated thermal power

RWP

radiation work permit

SBLC

standby liquid control

SDP

significance determination process

SR

surveillance requirement

SRV

safety/relief valve

SSCs

structures, systems, and components

ST

surveillance test

TS

technical specification

UFSAR

Updated Final Safety Analysis Report

UT

ultrasonic testing

VHRA

very high radiation area

VT

visual examination

WOs

work orders