ML091200497

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IR 05000335-09-002, 05000389-09-002, on January 1 to March 31, 2009, St. Lucie Nuclear Plant - NRC Integrated Inspection Report
ML091200497
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 04/30/2009
From: Marvin Sykes
NRC/RGN-II/DRP/RPB3
To: Nazar M
Florida Power & Light Co
References
IR-09-002
Download: ML091200497 (33)


See also: IR 05000335/2009002

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

SAM NUNN ATLANTA FEDERAL CENTER

61 FORSYTH STREET, SW, SUITE 23T85

ATLANTA, GEORGIA 30303-8931

April 30, 2009

Mr. Mano Nazar

Executive Vice President, Nuclear and Chief Nuclear Officer

Florida Power and Light Company

P.O. Box 14000

Juno Beach, FL 33408-0420

SUBJECT:

ST. LUCIE NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT

05000335/2009002, 05000389/2009002

Dear Mr. Nazar:

On March 31, 2009, the US Nuclear Regulatory Commission (NRC) completed an inspection at

your St. Lucie Plant. The enclosed integrated inspection report documents the inspection

findings which were discussed on April 2, 2009, with Mr. Johnston and other members of your

staff.

The inspection examined activities conducted under your license as they related to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents three NRC identified findings and one self-revealing finding, all of very

low safety significance (Green). Additionally, one licensee-identified violation which was

determined to be of very low safety significance is listed in Section 4OA7 of this report. These

findings were determined to involve violations of NRC requirements. However, because of the

very low safety significance and because they are entered into your corrective action program,

the NRC is treating the findings as non-cited violations (NCVs) consistent with Section VI.A.1 of

the NRC Enforcement Policy. If you contest any NCV or disagree with an assigned cross-

cutting aspect in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial or disagreement, to the Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the

Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

St. Lucie facility. In addition, if you disagree with the characterization of any finding in this

report, you should provide a response within 30 days of the date of this inspection report, with

the basis for your disagreement, to the Regional Administrator, Region II, and the NRC

Resident Inspector at the St. Lucie Nuclear Plant. The information you provide will be

considered in accordance with Inspection Manual Chapter 0305

FP&L

2

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of the NRCs document

system (ADAMS). Adams is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Marvin D. Sykes, Chief

Rector Projects Branch 3

Division of Reactor Projects

Docket Nos.: 50-335, 50-389

License Nos.: DPR-67, NPF-16

Enclosure: Inspection Report 05000335/2009002, 05000389/2009002

w/Attachment: Supplemental Information

cc w/encl: (See page 3)

_________________________

XG SUNSI REVIEW COMPLETE

OFFICE

RII:DRP

RII:DRP

RII:DRP

RII:DRP

RII:DRS

SIGNATURE

JHamman for

MDS

TLH4

SPS

HGepford for

NAME

SNinh

MSykes

THoeg

SSanchez

LMiller

DATE

04/30/2009

04/30/2009

04/30/2009

04/30/2009

04/30/.2009

5/ /2009

5/ /2009

E-MAIL COPY?

YES

NO YES

NO YES

NO YES

NO YES

NO YES

NO YES

NO

FP&L

3

cc w/encl:

Gordon L. Johnston

Site Vice President

St. Lucie Nuclear Plant

Electronic Mail Distribution

Christopher R. Costanzo

Plant General Manager

St. Lucie Nuclear Plant

Electronic Mail Distribution

Mark Hicks

Operations Manager

St. Lucie Nuclear Plant

Electronic Mail Distribution

Eric Katzman

Licensing Manager

St. Lucie Nuclear Plant

Electronic Mail Distribution

Abdy Khanpour

Vice President

Engineering Support

Florida Power and Light Company

P.O. Box 14000

Juno Beach, FL 33408-0420

Robert J. Hughes

Director

Licensing and Performance Improvement

Florida Power & Light Company

Electronic Mail Distribution

Alison Brown

Nuclear Licensing

Florida Power & Light Company

Electronic Mail Distribution

M. S. Ross

Managing Attorney

Florida Power & Light Company

Electronic Mail Distribution

Marjan Mashhadi

Senior Attorney

Florida Power & Light Company

Electronic Mail Distribution

William A. Passetti

Chief

Florida Bureau of Radiation Control

Department of Health

Electronic Mail Distribution

Craig Fugate

Director

Division of Emergency Preparedness

Department of Community Affairs

Electronic Mail Distribution

J. Kammel

Radiological Emergency Planning

Administrator

Department of Public Safety

Electronic Mail Distribution

Mano Nazar

Senior Vice President and Nuclear Chief

Operating Officer

Florida Power & Light Company

Electronic Mail Distribution

Peter Wells

(Acting) Vice President, Nuclear

Training and Performance Improvement

Florida Power and Light Company

P.O. Box 14000

Juno Beach, FL 33408-0420

Mark E. Warner

Vice President

Nuclear Plant Support

Florida Power & Light Company

Electronic Mail Distribution

Faye Outlaw

County Administrator

St. Lucie County

Electronic Mail Distribution

Jack Southard

Director

Public Safety Department

St. Lucie County

Electronic Mail Distribution

FP&L

4

Letter to Mano Nazar from Marvin D. Sykes dated April 30, 2009

SUBJECT:

ST. LUCIE NUCLEAR PLANT - NRC INTEGRATED INSPECTION REPORT

05000335/2009002, 05000389/2009002

Distribution w/encl:

C. Evans, RII

L. Slack, RII

OE Mail

RIDSNRRDIRS

PUBLIC

RidsNrrPMStLucie Resource

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-335, 50-389

License Nos:

DPR-67, NPF-16

Report No:

05000335/2009002, 05000389/2009002

Licensee:

Florida Power & Light Company (FP&L)

Facility:

St. Lucie Nuclear Plant, Units 1 & 2

Location:

6351 South Ocean Drive

Jensen Beach, FL 34957

Dates:

January 1 to March 31, 2009

Inspectors:

T. Hoeg, Senior Resident Inspector

S. Sanchez, Resident Inspector

S. Ninh, Senior Project Engineer

L. Miller, Senior Reactor Inspector

R. Bernhard, Senior Reactor Analyst

Approved by:

M. Sykes, Chief

Reactor Projects Branch 3

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000335/2009-002, 05000389/2009-002; 01/01/2009 - 3/31/2009; St. Lucie Nuclear Plant,

Units 1 & 2; Event Follow-up, Other Activities, Surveillance Testing, Identification and

Resolution of Problems.

The report covered a three month period of inspection by resident inspectors and several region

based inspectors. The significance of most findings is identified by their color (Green, White,

Yellow, Red) using IMC 0609, Significance Determination Process (SDP). Findings for which

the SDP does not apply may be Green or be assigned a severity level after NRC management

review. The NRCs program for overseeing the safe operation of commercial nuclear power

reactors is described in NUREG-1649, Reactor Oversight Process, and Revision 4, dated

December 2006.

A.

Inspector Identified & Self-Revealing Findings

Cornerstone: Initiating Events

Green. A self-revealing finding was identified for failure to implement adequate process

controls to minimize risk during maintenance on the Unit 2, 5B feedwater heater high

level limit switch resulting in a manual reactor trip on June 4, 2008. No violations of

NRC requirements were identified because the feedwater heater drain system is non-

safety related. The licensee entered the issue into the corrective action program as

condition report (CR) 2008-18858. Corrective actions included development of specific

procedural direction for controlling and insulating energized control circuit leads during

work evolutions using the risk management process, design modifications to address

vulnerability when performing maintenance on level switches, and evaluation of industry

best practices for training and handling of energized leads.

The finding was more than minor because it resulted in a manual reactor trip. The

finding was associated with the human performance attribute and affected the Initiating

Events cornerstone objective of limiting the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown as well as at power

operations. Using the NRC Manual Chapter 0609, ASignificance Determination

Process,@ Attachment 609.04, Phase 1 screening worksheet, the finding was determined

to be of very low safety significance because it was a transient initiator but did not

increase the likelihood that mitigation equipment would not be available. The cause of

the finding is related to the cross-cutting area of Human Performance, with a work

control component. Specifically, the licensee did not adequately plan work activities to

minimize the risk of grounding the energized leads (H.3(a)). (Section 4OA3).

Cornerstone: Mitigating Systems

Green. The inspectors identified a Green noncited violation of Technical Specifications 3.8.1, AC Sources, for failure to perform a required monthly surveillance test in its

entirety. Specifically, the inspectors identified that St. Lucie has not performed Unit 1

Emergency Diesel Generator (EDG) technical specification (TS) surveillance

requirement 4.8.1.1.2 as written to verify the fuel oil transfer pumps will transfer fuel from

3

Enclosure

the storage tank to the engine mounted day tanks at least every 31 days to demonstrate

operability. The licensee entered the finding in their CAP as CR 2009-4976.

The finding is more than minor in accordance with Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening. Specifically, it

impacts the mitigating systems cornerstone objective in that it affects the operability,

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences. Using Manual Chapter 0609, Significance

Determination Process, Phase 1 worksheet, this finding was determined to be of very

low safety significance since it did not represent an actual loss of a safety function. The

inspectors determined that the cause of this finding has a crosscutting aspect in the area

of human performance associated with the resources attribute, in that the operators did

not have adequate procedural guidance available to completely test the fuel oil transfer

system as required by technical specifications. (IMC 0305 aspect H.2.c). (Section

1R22)

Green. The inspectors identified a NCV of TS 6.8.1.a and Regulatory Guide (RG) 1.33,

for the licensee failing to specify and ensure an appropriate post maintenance test

(PMT) was performed as required by administrative procedure ADM-78.01, Post

Maintenance Testing. Specifically, the inspectors identified that after replacement of an

emergency diesel generator (EDG) fuel oil day tank low level instrument, an inadequate

PMT was performed because the instrument switch mechanism was not demonstrated

functional by actual lowering of the fuel oil level within the tank to actuate the float

assembly. The licensee entered the finding in their CAP as CR 2008-32722.

The finding is more than minor because it is associated with the equipment performance

attribute of the mitigating systems cornerstone. The finding was determined to have

very low safety significance because it did not result in an actual loss of safety system

function. This finding was related to the coordination of work activities attribute of the

human performance cross-cutting area in the aspect of work control (IMC 0305 aspect

H.3.b). (Section 4OA5.3)

Green. The inspectors identified a Non Cited Violation (NCV) of 10 CFR 50, Appendix

B, Criterion XVI, Corrective Action, for failure of the licensee to take timely and effective

corrective actions to prevent recurrence of Unit 1 emergency diesel generator (EDG) day

tank low level switch failures starting in 2007. Specifically, in June 2007, the licensee

performed an apparent cause evaluation of sticking level switches and determined that

a manufacturing defect associated with the packing gland of the floats pivot shaft

caused some restricted movement. The licensee also determined that extended shelf

life contributed to the failures of these level switches. However, other than replacing the

switches with new ones, the only corrective action(s) that resulted from this evaluation

were to ensure that switches manufactured before 2000 were not used for plant

applications. Subsequently, in October 2008, the 1A-EDG day tank low level switch

failed during the 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> EDG run and again failed during maintenance activities in

February 2009.

4

Enclosure

The finding is more than minor because it is associated with the equipment performance

attribute of the mitigating systems cornerstone. The finding was determined to have

very low safety significance because an SDP Phase 3 analysis determined that the risk

was less than 1E-6/year. This finding was related to the corrective action attribute of the

problem identification and resolution cross-cutting area in the aspect of appropriate and

timely corrective actions (IMC 0305 aspect P.1.d). (Section 4OA2.3)

B.

Licensee Identified Violations

One violation of very low safety significance was identified by the licensee and has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into their corrective action program. This violation and corrective actions

are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

Summary of Plant Status:

Unit 1 and Unit 2 began the period at full Rated Thermal Power (RTP) and operated at full

power for most of the entire period. Unit 2 had an unplanned down power to 60 percent rated

thermal power to repair a turbine building cooling water pump bearing on March 5, 2009. Unit 2

returned to full power operation on March 10, 2009. Unit 2 reduced power to 85 percent rated

thermal power due to a traveling screen failure March 25, 2009. Unit 2 returned to full power

operation on March 30, 2009.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity (Reactor-R)

1R01 Adverse Weather Protection

a.

Inspection Scope

During the weeks of January 21 and February 2, 2009, the inspectors reviewed the

status of licensee actions in accordance with ADM-04.03, Cold Weather Preparations.

The inspectors verified conditions were met for entering the procedure and that

equipment status was verified as directed by the procedure. The inspectors performed a

walkdown of the following safety-related equipment on both units that are exposed to the

outside weather conditions to identify any potential adverse conditions. Condition

reports (CRs) were checked to assure that the licensee was identifying and resolving

weather related issues.

Unit 2 Emergency Diesel Generator (EDG) Rooms

Unit 1 C Auxiliary Feedwater (AFW) Pump Area

Unit 2 Main Feedwater Isolation Valve Area

Unit 1 Condensate Storage Tank Area

Unit 1 EDG Rooms

Unit 1 Refueling Water Tank (RWT)

Unit 2 RWT

b.

Findings

No findings of significance were identified.

6

Enclosure

1R04 Equipment Alignment

.1

Partial Equipment Walkdowns

a.

Inspection Scope

The inspectors conducted four partial alignment verifications of the safety-related

systems listed below. These inspections included reviews using plant lineup

procedures, operating procedures, and piping and instrumentation drawings, which were

compared with observed equipment configurations to verify that the critical portions of

the systems were correctly aligned to support operability. The inspectors also verified

that the licensee had identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers by

entering them into the corrective action program (CAP).

1B EDG while the 1A EDG was Out of Service (OOS)

2A Component Cooling Water (CCW) System while the 2B CCW System OOS

2B Containment Spray (CS) System while the 2A CS System OOS

1B and 2B Startup Transformers while the 1A and 2A Startup Transformers OOS

b.

Findings

No findings of significance were identified.

1R05 Fire Protection

a.

Inspection Scope

.1

Fire Area Walkdowns

The inspectors toured the following five plant areas during this inspection period to

evaluate conditions related to control of transient combustibles and ignition sources, the

material condition and operational status of fire protection systems including fire barriers

used to prevent fire damage or fire propagation. The inspectors reviewed these

activities against provisions in the licensees procedure ADM-1800022, Fire Protection

Plan, and 10 CFR Part 50, Appendix R. The licensees fire impairment lists, updated on

an as-needed basis, were routinely reviewed. In addition, the inspectors reviewed the

CR database to verify that fire protection problems were being identified and

appropriately resolved. The following areas were inspected:

Unit 1 Charging Pump Areas

Unit 1 Elevation -0.5 Pipe Penetration Area

Unit 2 Electrical Penetration Rooms

Unit 2 Control Element Drive Mechanism Control System Room

Unit 2 Emergency Core Cooling System (ECCS) Pumps Room

7

Enclosure

b.

Findings

No findings of significance were identified.

.2

Fire Protection - Drill Observation

a.

Inspection Scope

The inspectors observed a fire drill conducted in the Unit 1 Turbine Building 19.5'

Elevation 1C AFW Pump Room on January 20, 2009. The drill was observed to

evaluate the overall readiness of the plant fire brigade to respond to and extinguish fires.

The inspectors verified that the licensee staff identified deficiencies, openly discussed

them in a self-critical manner at the drill debrief, and took appropriate corrective actions

as required. Specific attributes evaluated were: (1) proper wearing of turnout gear and

self-contained breathing apparatus; (2) proper use and layout of fire hoses; (3)

employment of appropriate fire fighting techniques; (4) sufficient fire fighting equipment

brought to the scene; (5) effectiveness of command and control; (6) search for victims

and propagation of the fire into other plant areas; (7) smoke removal operations; (8)

utilization of pre-planned strategies; (9) adherence to the pre-planned drill scenario; and

(10) drill objectives.

b.

Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Training Program

Resident Inspector Quarterly Review

a.

Inspection Scope

On March 30, 2009, the inspectors observed and assessed licensed operator actions

during a simulated steam generator tube leak and subsequent reactor trip with

complications, to verify that operator performance was adequate and that evaluators

were identifying and documenting crew performance problems. The exercise was

performed in accordance with St. Lucie Plant Simulator Exercise Guide 0815018,

Revision 14. The inspectors also reviewed simulator physical fidelity and specifically

evaluated the following attributes related to the operating crews performance:

Clarity and formality of communication

Ability to take timely action to safely control the unit

Prioritization, interpretation, and verification of alarms

Correct use and implementation of off-normal and emergency operation procedures;

and emergency plan implementing procedures

Control board operation and manipulation, including high-risk operator actions

8

Enclosure

Oversight and direction provided by supervision, including ability to identify and

implement appropriate technical specification actions, regulatory reporting

requirements, and emergency plan classification and notification

Crew overall performance and interactions

Effectiveness of the post-evaluation critique.

b.

Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a.

Inspection Scope

The inspectors reviewed system performance data and associated CRs for the two

systems listed below to verify that the licensees maintenance efforts met the

requirements of 10 CFR 50.65 (Requirements for Monitoring the Effectiveness of

Maintenance at Nuclear Power Plants) and licensee Administrative Procedure ADM-17-

08, Implementation of 10CFR50.65, Maintenance Rule. The inspectors efforts focused

on maintenance rule scoping, characterization of maintenance problems and failed

components, risk significance, determination of a(1) and a(2) classification, corrective

actions, and the appropriateness of established performance goals and monitoring

criteria. The inspectors also interviewed responsible engineers and observed some of

the corrective maintenance activities. The inspectors also attended applicable expert

panel meetings and reviewed associated system health reports. The inspectors verified

that equipment problems were being identified and entered into the CAP

Unit 1 Emergency Diesel Generator System

Unit 1 Intake Cooling Water System

b.

Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Control

a.

Inspection Scope

The inspectors completed in-office reviews, plant walkdowns, and control room

inspections of the licensees risk assessment of six emergent or planned maintenance

activities. The inspectors verified the licensees risk assessment and risk management

activities using the requirements of 10 CFR 50.65(a)(4); the recommendations of

Nuclear Management and Resource Council 93-01, Industry Guidelines for Monitoring

the Effectiveness of Maintenance at Nuclear Power Plants, Revision 3; and procedure

ADM-17.16, Implementation of the Configuration Risk Management Program. The

inspectors also reviewed the effectiveness of the licensees contingency actions to

mitigate increased risk resulting from the degraded equipment. The inspectors

9

Enclosure

interviewed responsible Senior Reactor Operators on-shift, verified actual system

configurations, and specifically evaluated results from the online risk monitor (OLRM) for

the combinations of out of service (OOS) risk significant systems, structures, and

components (SSCs) listed below:

1A HPSI Pump, Valve HCV-3627, and Fan HVS-5A OOS

1B LPSI Pump, Valve SB-37-2, and 1A AFW Pump OOS

2B Emergency Core Cooling System (ECCS) OOS

2A ECCS OOS

1A EDG, 1C Instrument Air Compressor, and Valve PCV-8805 OOS

1B EDG and Valve HCV-08-2B OOS

b.

Findings

No findings of significance were identified.

1R15 Operability Evaluations

a.

Inspection Scope

The inspectors reviewed the following six CR interim dispositions and operability

determinations to ensure that operability was properly supported and the affected SSCs

remained available to perform its safety function with no increase in risk. The inspectors

reviewed the applicable UFSAR, and associated supporting documents and procedures,

and interviewed plant personnel to assess the adequacy of the interim disposition.

CR 2009-2369, 1A EDG Sump Oil Temperature

CR 2009-1471, Unit 2 ECCS Piping Insulation Removed

CR 2009-2825, CEA # 85 Placed on the Lower Gripper

CR 2009-5595, 1A EDG Air Intake Screen Corroded

CR 2009-6666, 1A LPSI System Piping Air Voiding

CR 2009-2951, Unit 2 Safety Injection Tank Sample Valve Operation

b.

Findings

No findings of significance were identified

1R18 Plant Modifications

a.

Inspection Scope

The inspectors reviewed the documentation for a permanent modification affecting both

units, plant change modification PCM 07127, ECCS Piping Insulation Modification to

Support Void Inspections. The inspectors reviewed the 10 CFR 50.59 screening and

evaluation, fire protection review, environmental review, As Low As Reasonably

Achievable (ALARA) screening, and license renewal review, to verify that the

modification had not affected system operability/availability. The inspectors reviewed

10

Enclosure

associated plant drawings and UFSAR documents impacted by this modification and

discussed the changes with licensee personnel to verify that the installation was

consistent with the modification documents. Additionally, the inspectors verified that

problems associated with modifications were being identified and entered into the CAP.

b.

Findings

No findings of significance were identified.

1R19 Post Maintenance Testing

a.

Inspection Scope

For the five post maintenance tests (PMTs) listed below, the inspectors reviewed the test

procedures and either witnessed the testing and/or reviewed test records to determine

whether the scope of testing adequately verified that the work performed was correctly

completed and demonstrated that the affected equipment was functional and operable.

The inspectors verified that the requirements of procedure ADM-78.01, Post

Maintenance Testing, were incorporated into test requirements. The inspectors

reviewed the following work orders (WOs) and/or work requests (WR):

WO 38000129, Valve MV-07-2A Stroke Test and Dynamic Analysis

WO 39002591, 1A EDG Day Tank Level Switch Replacement

WO 37014539, 1B EDG Day Tank Level Switch Replacement

WO 39002134, 1A EDG Lube Oil Line Replacement

WO 38027005, Valve HCV-09-18 Oil Replacement

b.

Findings

No findings of significance were identified.

1R22 Surveillance Testing

a.

Inspection Scope

The inspectors either reviewed or witnessed the following six surveillance tests to verify

that the tests met the TS, the UFSAR, the licensees procedural requirements, and

demonstrated the systems were capable of performing their intended safety functions

and their operational readiness. In addition, the inspectors evaluated the effect of the

testing activities on the plant to ensure that conditions were adequately addressed by

the licensee staff and that after completion of the testing activities, equipment was

returned to the positions/status required for the system to perform its safety function.

The tests reviewed included one in-service test and two containment isolation valve

surveillances. The inspectors verified that surveillance issues were documented in the

CAP.

11

Enclosure

2-OSP-59.01A, 2A EDG Monthly Test

2-OSP-69.25, Unit 2 Engineered Safeguards Testing

1-OSP-59.01A, 1A EDG Monthly Test

OP-2-0010125A, Valve MV-07-2B Stroke Test

1-OSP-66.01, Unit 1 Control Element Assembly Exercise

1-OSP-9.01A, 1A AFW Pump Code Run

b.

Findings

Introduction. The inspectors identified a Green noncited violation of Technical

Specifications (TS) 3.8.1, AC Sources, for failure to perform a required monthly

surveillance test in its entirety. Specifically, the inspectors identified that St. Lucie has

not performed Unit 1 EDG TS surveillance requirement 4.8.1.1.2 as written to verify the

fuel oil transfer pumps will transfer fuel from the storage tank to the engine mounted day

tanks at least every 31 days to demonstrate operability.

Description. During the month of January, 2009, the inspectors reviewed the Unit 1

EDG monthly surveillance test procedures 1-OSP-59.01A and 1-OSP-59.01B, 1A

Emergency Diesel Generator Monthly Surveillance and 1B Emergency Diesel Generator

Monthly Surveillance prior to performing planned inspections. The inspectors

determined that procedure section 7.1 started the fuel oil transfer pump while it was

lined up in the recirculation mode to the fuel oil storage tank and did not transfer fuel to

the engine mounted day tank. The inspector concluded a verification of the pumps

ability to transfer fuel to the day tank had not been performed on a monthly basis as

required by technical specifications. The St. Lucie TS surveillance section 4.8.1.1.2 is

required to be performed as written to verify the fuel oil transfer pumps can be started

and transfer fuel from the storage tank to the engine mounted day tanks at least every

31 days to demonstrate operability.

The inspector reviewed past Unit 1 EDG monthly surveillance tests to determine if the

method of testing the fuel oil transfer pump for operability had been revised since the

plant started commercial operation in 1976. The inspector found that before 1993, the

Unit 1 EDG periodic test required by visual observation that the EDG fuel oil transfer

pump runs and actually increases level in the generator mounted tanks. In 1993, the

subject surveillance procedures were revised to run the fuel oil transfer pump in the

recirculation mode and verifying the pump discharge pressure measured a minimum of

25 psig while the fuel oil is pumped from the storage tanks back to the storage tank

versus the generator engine mounted day tanks as previously required. The practice of

not transferring fuel with the transfer pump to the day tank on a monthly basis reduced

the licensees ability to identify pump degradation and/or capability, rendering the EDGs

not fully reliable to meet a mission time of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The inspectors determined that the

test procedure revision and methodology of periodically testing the operation of the fuel

oil transfer system was inadequate and may not verify full operability of the fuel oil

transfer system.

12

Enclosure

The inspectors shared their findings with the licensee and informed them that their

practice of testing the pump in the recirculation mode without verifying the transfer of fuel

to the engine mounted tank did not meet technical specification monthly surveillance test

requirements. The licensee entered the condition in their CAP as CR 2009-4976 and

took prompt action to verify compliance with the TS requirements over a two week

period. The Unit 1 EDG surveillance of the fuel oil transfer systems were tested

satisfactorily and monthly surveillance test procedures 1-OSP-59.01A and 1-OSP-

59.01B were revised to reflect the monthly TS surveillance requirement by returning to

the method of testing used before 1993 to determine operability.

Analysis. The inspectors determined that failure to perform a required TS surveillance in

its entirety is a performance deficiency. The finding is more than minor in accordance

with Inspection Manual Chapter (IMC) 0612, Power Reactor Inspection Reports,

Appendix B, Issue Screening. Specifically, the finding impacts the mitigating systems

cornerstone objective in that it affects the operability, availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences. Using Manual Chapter 0609, Significance Determination Process,

Phase 1 worksheet, this finding was determined to be of very low safety significance

since it did not represent an actual loss of a safety function. The inspectors determined

that the cause of this finding has a crosscutting aspect in the area of human

performance associated with the resources attribute, in that the operators did not have

adequate procedural guidance available to completely test the fuel oil transfer system as

required by technical specifications. (MC 0305 aspect H.2.c).

Enforcement. TS 3.8.1 requires surveillance requirement 4.8.1.1.2.3.a.3 to be

performed for each diesel generator to demonstrate operability on a monthly basis.

Contrary to this requirement, the licensee failed to perform TS surveillance requirement 4.8.1.1.2.3.a since 1993. The surveillance procedure was revised in 1993 and that

method used to test the fuel oil transfer system remained in use for over 15 years and

became an accepted practice by the licensee. Since the licensee entered the issue into

their CAP as CR 2009-4976 and the finding is of very low safety significance (Green),

this violation is being treated as a noncited violation, consistent with Section VI.A of the

NRC Enforcement Policy: NCV 05000335/2009002-01: Failure to Perform a Required

TS Surveillance.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Testing

a.

Inspection Scope

The inspector evaluated the adequacy of licensee=s methods for testing the alert and

notification system in accordance with NRC Inspection Procedure 71114, Attachment

02, AAlert and Notification System Evaluation@. The applicable planning standard 10

CFR Part 50.47(b)(5) and its related 10 CFR Part 50, Appendix E, Section IV.D

requirements were used as reference criteria. The criteria contained in NUREG-0654,

ACriteria for Preparation and Evaluation of Radiological Emergency Response Plans and

13

Enclosure

Preparedness in Support of Nuclear Power Plants,@ Revision 1, was also used as a

reference.

The inspector reviewed various documents which are listed in the Attachment to this

report. This inspection activity satisfied one inspection sample for the alert and

notification system on a biennial basis.

b.

Findings

No findings of significance were identified.

1EP3 Emergency Response Organization (ERO) Augmentation

a.

Inspection Scope

The inspector reviewed the licensee=s Emergency Response Organization (ERO)

augmentation staffing requirements and process for notifying the ERO to ensure the

readiness of key staff for responding to an event and timely facility activation. The

qualification records of key position ERO personnel were reviewed to ensure all ERO

qualifications were current. A sample of problems identified from augmentation drills or

system tests performed since the last inspection were reviewed to assess the

effectiveness of corrective actions.

The inspection was conducted in accordance with NRC Inspection Procedure 71114,

Attachment 03, AEmergency Response Organization Staffing and Augmentation

System.@ The applicable planning standard, 10 CFR 50.47(b)(2) and its related 10 CFR

50, Appendix E requirements were used as reference criteria.

The inspector reviewed various documents which are listed in the Attachment to this

report. This inspection activity satisfied one inspection sample for the ERO staffing and

augmentation system on a biennial basis.

b.

Findings

No findings of significance were identified.

1EP4 Emergency Action Level (EAL) and Emergency Plan Changes

a.

Inspection Scope

Since the last NRC inspection of this program area, Revisions 52, 53 and 54 of the

Emergency Plan was implemented based on the licensees determination, in accordance

with 10 CFR 50.54(q), that the changes resulted in no decrease in the effectiveness of

the Plan, and that the revised Plan continued to meet the requirements of 10 CFR

50.47(b) and Appendix E to 10 CFR Part 50. The inspector conducted a sampling

review of the Plan changes and implementing procedure changes made between

January 1, 2008 and January, 2009 to evaluate for potential decreases in effectiveness

of the Plan. However, this review was not documented in a Safety Evaluation Report

14

Enclosure

and does not constitute formal NRC approval of the changes. Therefore, these changes

remain subject to future NRC inspection in their entirety.

The inspection was conducted in accordance with NRC Inspection Procedure 71114,

Attachment 04, AEmergency Action Level and Emergency Plan Changes.@ The

applicable planning standard (PS), 10 CFR 50.47(b)(4) and its related 10 CFR 50,

Appendix E requirements were used as reference criteria.

The inspector reviewed various documents which are listed in the Attachment to this

report. This inspection activity satisfied one inspection sample for the emergency action

level and emergency plan changes on an annual basis.

b.

Findings

No findings of significance were identified.

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies

a.

Inspection Scope

The inspector reviewed the corrective actions identified through the Emergency

Preparedness program to determine the significance of the issues and to determine if

repeat problems were occurring. The facility=s self-assessments and audits were

reviewed to assess the licensee=s ability to be self-critical, thus avoiding complacency

and degradation of their emergency preparedness program. In addition, the inspector

reviewed licensee self-assessments and audits to assess the completeness and

effectiveness of all emergency preparedness related corrective actions.

The inspection was conducted in accordance with NRC Inspection Procedure 71114,

Attachment 05, ACorrection of Emergency Preparedness Weaknesses.@ The applicable

planning standard, 10 CFR 50.47(b)(14) and its related 10 CFR 50, Appendix E

requirements were used as reference criteria.

The inspector reviewed various documents which are listed in the Attachment to this

report. This inspection activity satisfied one inspection sample for the correction of

emergency preparedness weaknesses on a biennial basis.

b.

Findings

No findings of significance were identified.

15

Enclosure

OTHER ACTIVITIES

4OA1 Performance Indicator Verification

.1

Initiating Events and Mitigating Systems Cornerstones

a.

Inspection Scope

The inspectors checked licensee submittals for the performance indicators (PIs) listed

below for the period January 2008 through December 2008, to verify the accuracy of the

PI data reported during that period. Performance indicator definitions and guidance

contained in NEI 99-02, Regulatory Assessment Performance Indicator Guideline, and

licensee procedures ADM-25.02, NRC Performance Indicators, and NAP-206, NRC

Performance Indicators, were used to check the reporting for each data element. The

inspectors checked operator logs, plant status reports, CRs, system health reports, and

PI data sheets to verify that the licensee had identified the required data, as applicable.

The inspectors interviewed licensee personnel associated with performance indicator

data collection, evaluation, and distribution.

Unit 1 Unplanned Scrams per 7000 Critical Hours

Unit 2 Unplanned Scrams per 7000 Critical Hours

Unit 1 Unplanned Scrams With Loss of Normal Heat Removal

Unit 2 Unplanned Scrams With Loss of Normal Heat Removal

Unit 1 Unplanned Transients per 7000 Critical Hours

Unit 2 Unplanned Transients per 7000 Critical Hours

b.

Findings

No findings of significance were identified.

.2

Emergency Preparedness Cornerstones

a.

Inspection Scope

The inspector sampled licensee submittals relative to the PIs listed below for the period

January 2008 through December 2008. To verify the accuracy of the PI data reported

during that period, PI definitions and guidance contained in NEI 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 5, was used to confirm the

reporting basis for each data element.

Emergency Response Organization (ERO) Drill/Exercise Performance

ERO Drill Participation

Alert and Notification System Reliability

For the specified review period, the inspector examined data reported to the NRC,

procedural guidance for reporting PI information, and records used by the licensee to

identify potential PI occurrences. The inspector verified the accuracy of the PI for ERO

16

Enclosure

drill and exercise performance through review of a sample of drill and event records.

The inspector reviewed selected training records to verify the accuracy of the PI for ERO

drill participation for personnel assigned to key positions in the ERO. The inspector

verified the accuracy of the PI for alert and notification system reliability through review

of a sample of the licensees records of periodic system tests. The inspector also

interviewed the licensee personnel who were responsible for collecting and evaluating

the PI data. Licensee procedures, records, and other documents reviewed within this

inspection area are listed in the Attachment to this report.

b.

Findings

No findings of significance were identified.

4OA2 Problem Identification and Resolution

.1

Daily Review

a.

Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and to help identify repetitive equipment failures or specific human performance issues

for follow-up, the inspectors performed a screening of items entered daily into the

licensees CAP. This review was accomplished by reviewing daily printed summaries of

CRs and by reviewing the licensees electronic CR database. Additionally, reactor

coolant system unidentified leakage was checked on a daily basis to verify no

substantive or unexplained changes.

b. Findings

No findings of significance were identified.

.2

Annual Sample. 1B1 Reactor Coolant Pump Seal Flanges Found Removed With

Danger Tags Still Attached

a.

Inspection Scope

The inspectors selected CR 2008-35071, 1B1 Reactor Coolant Pump Seal Flanges

Found Removed With Danger Tags Still Attached, for a more in-depth review of the

circumstances that led up to the equipment clearance order (ECO) mishap and the

corrective actions that followed.

The inspectors reviewed the licensees evaluation of the event and the associated

corrective actions. The inspectors reviewed the apparent cause evaluation and

interviewed plant personnel. The inspectors evaluated the licensees administration of

this selected condition report in accordance with their CAP as specified in licensee

procedures PI-AA-204, Condition Identification and Screening Process, and PI-AA-205,

Condition Evaluation and Corrective Actions.

17

Enclosure

b.

Findings and Observations

On November 11, 2008, while Unit 1 was defueled during a refueling outage a

maintenance crew entered containment to begin work on installing new reactor coolant

pump (RCP) seal injection piping. The equipment clearance order (ECO) tags were still

hanging on the blank flanges that were in place to provide system boundary protection

while the new piping was being fabricated. In preparation of installing the new piping,

the workers proceeded to remove the flanges with the danger tags still attached. This

was in contrast to licensee procedure ADM-09.04, In-Plant Equipment Clearance

Orders Section 6.2, step 3.a which required at no time shall an ECO tag be removed or

ignored. The inspectors determined the apparent cause analysis of this event was

thorough and provided additional details of contributing causes. The corrective actions

taken by the licensee or planned were in accordance with their above referenced

procedures. This licensee identified finding involved a violation of TS 6.8.1, Procedures

and Programs. The enforcement aspects of this violation are discussed in Section 4OA7

of this report.

.3

Semi-Annual Trend Review

a.

Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

the inspectors reviewed the licensees CAP and associated documents to identify trends

that could indicate the existence of a more significant safety issue. The inspectors

selected Murphy switch failures for trending due to a number of recent failures

associated with the Unit 1 EDG fuel oil transfer system. The inspectors review was

focused on repetitive equipment issues, but also considered the results of daily inspector

CR item screening discussed in Section 4OA2.1 above, plant status reviews, plant tours,

document reviews, and licensee trending efforts. The inspectors review nominally

considered the six month period of July through December 2008. Corrective actions

associated with a sample of the issues identified in the licensees CAP were reviewed for

adequacy.

b.

Assessment and Observations

Introduction. The inspectors identified an Non Cited Violation (NCV) of 10 CFR 50,

Appendix B, Criterion XVI, Corrective Action, for the licensee failing to take timely and

effective corrective actions to prevent recurrence of Unit 1 emergency diesel generator

(EDG) day tank low level switch failures resulting in the 1A EDG being unreliable to meet

its continuous operational mission time of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Specifically, multiple repeat switch

failures occurred over a two year period where the cause of the failure was not identified

and corrected to prevent recurrence.

Description. The St. Lucie Unit 1 EDGs have engine skid mounted day tanks supplied

by a larger external storage tank for fuel supply during extended periods of operation.

The day tank fuel oil inventory is controlled by use of several Murphy level switches.

The switch design consists of a reservoir and float mechanism assembly that moves with

level changes in the day tank to actuate a micro switch which in turn controls alarms,

18

Enclosure

pumps, and valve operation to maintain an adequate fuel oil inventory in the day tank.

On June 11, 2007, CR 2007-17693 was written identifying a condition where the 1A

EDG day tank high level switch LS-59-007A failed to actuate on an increasing level

following maintenance activities. The licensee documented the cause of this failure to

be a manufacturing defect causing the switch to stick. The corrective action replaced

the switch with a new one. On October 22, 2008, CR 2008-32418 was written identifying

a condition where the 1A EDG day tank low level switch LS-59-008A failed to actuate on

a lowering level during the 24-hour run of the diesel. The licensee documented the

cause of this failure to be the float mechanism lever arm binding and not actuating the

micro switch. The corrective action replaced the switch with a new one. On February 9,

2009, CR 2009-3756 was written identifying a condition where the 1A EDG low level

switch LS-59-008A again failed to actuate on a lowering level, this time following online

maintenance activities. On February 16, 2009, CR 2009-4456 was written identifying a

condition where the 1B EDG low-low level switch LS-59-010B failed to actuate on a

lowering level following maintenance activities. Following this last failure, the licensee

acknowledged a trend and established a root cause team to evaluate the failures.

In the June 2007 failure, the 1A EDG day tank high level switch (LS-59-007A) failed and

the low level switch (LS-59-008A) was thought to have been sticking. The licensee

performed an apparent cause evaluation of sticking level switches and determined that

a manufacturing defect associated with the packing gland of the floats pivot shaft

caused some restricted movement. The licensee also determined that extended shelf

life contributed to the failures of these level switches. However, other than replacing the

switches with new ones, the only corrective action(s) that resulted from this evaluation

were to ensure that switches manufactured before 2000 were not used for plant

applications. In the October 2008 failure, the 1A EDG day tank low level switch (LS-59-

008A) failed during the 24-hour EDG run. Unit 1 was in a refuel outage at the time and

only one EDG was required to be operable in accordance with TS. The failed level

switch was sent out for a third-party evaluation but the immediate corrective action was

to replace with a new switch and perform an adequate post maintenance test. The third-

party evaluation subsequently came back indeterminate for root cause. In the February

2009 failure, the 1A EDG day tank low level switch (LS-59-008A) again failed following

maintenance activities and a week later the 1B EDG day tank low-low level switch (LS-

59-010B) failed following its maintenance. At the conclusion of this inspection period,

the licensee was completing a root cause evaluation for Murphy level switch failures.

Analysis. The finding was determined to be more than minor because it affected the

Mitigating Systems Cornerstone objective to ensure the availability, reliability, and

capacity of systems that respond to initiating events to prevent undesirable

consequences. The finding was evaluated in accordance with NRC Inspection Manual

Chapter 0609.04, Significance Determination Process (SDP) Phase 1 screening

worksheets. Because it represented an actual loss of the EDG system safety function of

a single train for greater than its Technical Specification (TS) allowed outage time, SDP

Phase 2 worksheets were evaluated. The finding was determined to be potentially

greater than Green because the 1A EDG was inoperable since June 2007 and no

operator recovery credit was allowed. An SDP Phase 3 analysis was performed for the

deficiency. The NRC's risk model was modified to increase the EDG failure rate on Unit

1 to reflect the decrease in reliability of the switches. The resulting analysis, including

19

Enclosure

the risk contribution due to external sources, was slightly less than 1E-6/year and the

finding is GREEN. The analysis showed the plant is very sensitive to changes in

reliability of the switches. Insights gained from the review of the performance deficiency

by the licensee resulted in recommended changes to the type of switches used, and

corrections to the alarm response procedure used to respond to fuel related diesel

issues. The inspectors determined that the cause of this finding was related to the

appropriate and timely corrective actions aspect of the corrective action program

component in the problem identification and resolution cross-cutting area (P.1 (d)).

Enforcement. Criterion XVI of 10 CFR 50, Appendix B, states in part, that Measures

shall be established to assure that conditions adverse to quality, such as failures,

malfunctions, deficiencies, deviations, defective material and equipment, and

nonconformances are promptly identified and corrected. Contrary to this requirement,

the licensee failed to take timely and effective corrective actions to prevent recurrence of

Unit 1 EDG day tank low level switch failures resulting in the 1A-EDG being inoperable

since 2007. Because the licensee entered the issue into their CAP as CR 2009-3756

and the finding is Green, this violation is being treated as a NCV, consistent with Section

VI.A of the NRC Enforcement Policy: NCV 05000335/2009002-02: Failure to Take

Timely and Effective Corrective Actions for EDG Day Tank Level Switch Failure.

4OA3 Event Follow-up

.1

(Closed) LER 05000389/2008-002-00, Unit 2 Manually Tripped As A Result of

Maintenance.

a.

Inspection Scope

The inspectors reviewed the root cause evaluation associated with LER 05000589/2008-

002-00 to determine whether a performance deficiency was involved, corrective actions

were adequate and to determine the safety significance. The inspectors also reviewed

the LER to verify its accuracy and completeness.

b.

Findings

Introduction. A Green self-revealing finding was identified for failure to implement

adequate process controls to minimize risk during maintenance on the Unit 2, 5B

feedwater heater high level limit switch which resulted in a manual reactor trip on

June 4, 2008. No violations of NRC requirements were identified because the feedwater

heater drain system is non-safety related.

Description. On June 4, 2008, Unit 2 was in Mode 1 at 100% power, while instrument

and control ( I &C) personnel were performing maintenance on the 5B Feedwater (FW)

Heater High Level Limit Switch LS-11-26B, when two taped energized leads were being

routed through a conduit elbow came in contact with the conduit and grounded. The

ground resulted in the 2B Heater Drain Pump being tripped on low level and the 2A Main

Feedwater Pump tripping on low suction pressure 50 seconds after the heater drain

pump tripped. The reactor was manually tripped in anticipation of a low steam generator

level auto-trip. All safe shutdown equipment operated as designed.

20

Enclosure

The licensee determined the root cause of the event was a failure to implement

adequate process controls to minimize risk during level switch replacement and drifting

of the pressure switch set point causing a premature actuation of the switch during a

feed water transient. Corrective actions included a development of specific procedural

direction for controlling energized leads during work evolutions using the risk

management process, design modifications to address vulnerability when performing

maintenance on level switches, and evaluation of industry best practices for training and

handling of energized leads.

Analysis. The inspectors determined that failure to implement adequate process controls

to minimize risk during maintenance on the Unit 2, 5B feedwater heater high level limit

switch resulting in a manual reactor trip was a performance deficiency. Specifically, the

licensee did not adequately plan work activities to minimize the risk of grounding the

energized leads. The existing plant processes for assessment of such risk are

contained in ADM 00110432, Control of Plant Work Orders and WW-AA-1000, Work

Activity Risk Assessment Process. Since the original work scope was to correct a steam

leak, the ADM 0010432, Red Sheet did not apply. The Red Sheet is a stand alone work

control checklist used by plant personnel to determine if proposed power block and

switchyard work activities have potential to cause an actuation of an Engineered

Safeguards Feature (EFS), plant transient or a unit trip. However, when the scope of the

work order was expanded to include the feedwater heater level switch replacement, the

package was not revised and a formal risk assessment was not performed.

The finding was more than minor because it resulted in a manual reactor trip. The

finding was associated with the human performance attribute and affected the Initiating

Events cornerstone objective of limiting the likelihood of those events that upset plant

stability and challenge critical safety functions during shutdown as well as at power

operations. Using the NRC Manual Chapter 0609, ASignificance Determination

Process,@ Attachment 609.04, Phase 1 screening worksheet, the finding was determined

to be of very low safety significance because it was a transient initiator but did not

increase the likelihood that mitigation equipment would not be available. The cause of

the finding is related to the cross-cutting area of Human Performance, with a work

control component. Specifically, the licensee did not adequately plan work activities to

minimize the risk of grounding the energized leads (H.3(a)).

Enforcement. No violation of NRC regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because the performance

deficiency involved non-safety related equipment. This finding was determined to be of

very low safety significance (Green) and was entered into the corrective action program

as CR 2008-18858. This finding is identified as FIN 05000389/2009-02-04, Failure to

Implement Adequate Process Controls during Maintenance Activities Resulted in a

Manual Reactor Trip.

21

Enclosure

.2

(Closed) LER 05000389/2008-003-00: Unit 2 Condensate Pump Failure Resulting in

Manual Reactor Trip

The LER documented that while Unit 2 at 100 percent power, the 2B condensate pump

motor lead lugs overheated and melted due to high resistance at the lug crimp

connections which resulted in a manual reactor trip on June 7, 2008. The licensee

determined that the high resistance was caused by undetected epoxy resin in the motor

lead cables. The motor lead lugs were installed with undetected epoxy resin because a

vendor inadvertently impregnated the motor lead cables with epoxy resin during the

vacuum pressure impregnation (VIP) process. Corrective action included revising motor

rewinding specification to ensure that epoxy is not applied to the motor lead during the

vendors VIP process. The inspectors reviewed the LER and CR 2008-19114

documenting the event. The inspectors checked the accuracy and completeness of the

LER and the appropriateness of the licensees corrective actions. No findings of

significance or violations of NRC requirements were identified. This LER is closed.

4OA5 Other Activities

.1

Quarterly Resident Inspector Observation of Security Personnel and Activities

a.

Inspection Scope

During the inspection period the inspectors conducted observations of security force

personnel activities to ensure that the activities were consistent with the licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors normal plant status reviews and inspection activities.

b.

Findings

No findings of significance were identified.

.2

(Closed) NRC Temporary Instruction (TI) 2525/175, Emergency Response Organization,

Drill/Exercise Performance Indicator, Program Review

The inspector completed Temporary Instruction TI 2515/175, Emergency Response

Organization, Drill/Exercise Performance Indicator, Program Review. Appropriate

documentation of the results was provided to NRC, HQ, as required by the TI.

This completes the Region II inspection requirements for this TI for St. Lucie Plant.

.3

(Closed) URI 05000335/2008005-02: Failure of the Automatic Diesel Fuel Oil Transfer

System Could Potentially Result in the 1A EDG Being Inoperable

During the fourth quarter of 2008, the inspectors selected CR 2008-32418, 1A EDG

Fuel Oil Transfer Pump Did Not Start When Required, for a more in depth review. An

22

Enclosure

URI was identified by the inspectors relating to past operability of the EDG, adequacy of

post maintenance testing, and the capability to manually operate the fuel oil transfer

system as necessary to maintain system design functions. This review was completed

by the licensee during this inspection period and further reviewed and evaluated by the

inspectors as discussed in more detail in section 4OA2.3 of this report. This URI was

documented in NRC Report No. 05000335, 335/2008005 dated January 30, 2009.

Introduction. The inspectors identified a Green non-cited violation (NCV) of TS 6.8.1.a

and Regulatory Guide (RG) 1.33, for the licensee failing to properly plan and specify an

adequate post maintenance test (PMT) as required by safety related administrative

procedure ADM-78.01, Post Maintenance Testing. Specifically, the inspectors

identified that the 1A EDG fuel oil day tank low level Murphy switch was not

demonstrated fully functional prior to returning the EDG to service following maintenance

which is in contrast to PMT completion criteria required by ADM-78.01.

Description. In October, 2008, while reviewing CR 2008-32418, 1A-EDG Fuel Oil

Transfer Pump Did Not Start When Required, the inspectors determined that during the

TS required 24-hour surveillance run of the 1A EDG performed on October 22, 2008, the

licensee had to mechanically agitate the day tank low level switch LS-59-008A for the

fuel oil transfer pump to automatically start. The day tank low level switch in designed to

start the transfer pump and begin refilling the day tanks automatically. Design Basis

Document section 7.14.1 states, in part, that the EDG day tanks shall be provided with

level switches to automatically operate the transfer pumps and the solenoid isolation

valves.

Upon further review of the licensees CAP program, the inspectors discovered that LS-

59-008A had failed previously during a routine calibration in June of 2007, and was

replaced under WO 37012672. When the inspectors reviewed WO 37012672, it was

determined that the specified PMT did not completely test the level switch functionality.

The only test performed on the level switch was a resistance measurement taken to

ensure the electrical contacts on the micro switch worked properly when it was manually

opened and closed with a thumb screw by the maintenance technician. The mechanical

float assembly was not tested to ensure it actuates in response to a lowering tank level

as designed during normal operation. The inspectors determined that if the float

mechanism was defective or not responding properly, the specified PMT would not

identify the new switch as unreliable or defective. The licensee documented this issue in

their CAP as CR 2008-32722 to ensured that prior to returning the 1A EDG to service,

the day tank low level switch would be demonstrated functional by lowering the actual

level in the day tank and testing the entire switch assembly including the float

mechanism.

Analysis. The inspectors determined that the licensees failure to perform an adequate

1A EDG day tank level switch PMT as required by procedure ADM-78.01was a

performance deficiency creating an inability to identify a degraded switch which could fail

to actuate on an actual lowering level in the tank and not being able to perform its design

function. The inspectors concluded that the finding was more than minor in accordance

with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Disposition

Screening. The finding is associated with the equipment performance attribute of the

23

Enclosure

mitigating systems cornerstone. Using Manual Chapter 0609, Appendix A, Attachment

1, Significance Determination Process, Phase 1 Worksheet, the finding was

determined to have very low safety significance because it did not result in an actual loss

of a safety system function. The inspectors found that the cause of this finding was

related to the coordination of work activities aspect of the work controls component in

the human performance cross-cutting area (IMC 0305 aspect H.3.b).

Enforcement. TS 6.8.1.a requires that written procedures shall be established,

implemented, and maintained covering the activities specified in RG 1.33, Revision 2,

February 1978. RG 1.33, Appendix A, Item 9.a, requires maintenance that can affect

safety related equipment be properly preplanned and performed in accordance with

written instructions appropriate to the circumstances. Contrary to the above, PMT

requirements on the EDG fuel oil day tank low level switch were not adequately specified

and performed prior to returning the system to operable status in accordance with safety

related procedure ADM-78.01, Post Maintenance Testing. Because the failure to

implement the subject procedure was of very low safety significance and has been

entered in the licensees CAP, this violation is being treated as an NCV, consistent with

Section VI.A of the NRC Enforcement Policy: NCV 05000389/2009005-03, Failure to

Perform an Adequate Post Maintenance Test on the 1A-EDG Fuel Oil Day Tank Low

Level Switch.

3.

Closed) Temporary Instruction (TI) 2515/176, EDG TS Surveillance Requirements

Regarding Endurance and Margin Testing

a.

Inspection Scope

Inspection activities for TI 2515/176 were previously completed and documented in

inspection report 05000335, 389/2008004, and this TI is considered closed at St. Lucie

Nuclear Plant; however, TI 2515/176 will not expire until August 31, 2009. The

information gathered while completing this temporary instruction was forwarded to the

Office of Nuclear Reactor Regulation for review and evaluation.

b.

Inspection Findings

No findings of significance were identified.

4OA6 Exit

.1

Exit Meeting Summary

The resident inspectors presented the inspection results to Mr. Johnston and other

members of licensee management on April 2, 2009. The inspectors asked the licensee

whether any of the material examined during the inspection should be considered

proprietary information. The licensee did not identify any proprietary information.

24

Enclosure

.2

Annual Assessment Meeting Summary

On April 23, 2009, the Senior Resident Inspector met with Chris Costanzo and other

members of the licensee staff to discuss the NRCs annual assessment of the St. Lucie

Nuclear Plants safety performance for the period of January 1 through December 31,

2008. The annual assessment results were previously provided to Florida Power and

Light Company (FP&L) via letter dated March 4, 2009.

On April 29, 2009, the Chief of Reactor Projects Branch 3, the Resident Inspectors, and

Region II Public Affairs Officer held a Category 3 meeting for members of the public and

local officials. This Category 3 public meeting provided an open house public forum to

fully engage the public in a discussion of regulatory issues related to the NRCs ROP

and annual assessment of the St. Lucie Nuclear Plants safety performance for the

period January 1 through December 31, 2008. The presentation material used for

discussions and the list of attendees is available from the NRCs document system

(ADAMS) as accession number ML 090920483. ADAMS is accessible from the NRC

Web site at http://www/nrc.gov/reading-rm/adams.html (the Public Electronic Reading

Room).

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the

licensee and is a violation of NRC requirements which meets the criteria of Section VI of

the NRC Enforcement Policy, NUREG-1600, for being dispositioned as a NCV.

Technical Specification 6.8.1 requires that written procedures be implemented

covering activities referenced in RG 1.33, Revision 2, February 1978. Contrary to

this, on November 11, 2008, maintenance workers removed blank flanges on RCP

seal injection piping with danger tags still attached. The finding was more than minor

because it could be viewed as a precursor to a significant event and if left

uncorrected could lead to a more significant safety concern in that if plant personnel

remove, breach, or otherwise touch, plant equipment with danger tags attached, it

could result in an injury, death, or other unwanted consequences. The finding was

determined to be of very low safety significance because it only affected the initiating

events cornerstone for a loss of coolant accident initiator and could not have resulted

in exceeding the TS limit for RCS leakage since the reactor was defueled. The

licensee entered this issue into their CAP as CR 2008-35071.

ATTACHMENT: SUPPPLEMENTAL INFORMATION

Attachment

KEY POINTS OF CONTACT

Licensee personnel:

C. Ali, Licensing Engineer

E. Belizar, Projects Manager

M. Bladek, Assistant Operations Manager

D. Calabrese, Emergency Preparedness Supervisor

D. Cecchett, Licensing Engineer

J. Connor, Engineering Manager - Programs

T. Cosgrove, Site Engineering Director

C. Costanzo, Plant General Manager

A. Day, Chemistry Manager

M. Delowery, Maintenance Manager

S. Duston, Training Manager

K. Frehafer, Licensing Engineer

J. Heinold, Chemistry Technical Supervisor

M. Hicks, Operations Manager

D. Huey, Acting Work Control Manager

G. Johnston, Site Vice President

J. Klauck, Assistant Operations Manger

J. Kramer, Site Safety Manager

R. McDaniel, Fire Protection Supervisor

M. Moore, Radiation Protection Manager

P. Paradis, Fix-It-Now Team Supervisor

T. Patterson, Performance Improvement Department Manager

J. Porter, Design Engineering Manager

G. Swider, Systems and Component Engineering Manager

NRC personnel:

M. Sykes, Region II, Chief, Branch 3, Division of Reactor Projects

S. Ninh, Region II, Senior Project Engineer, Branch 3, Division of Reactor Projects

R. Bernhard, Region II, Senior Risk Analyst, Division of Reactor Projects

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

NONE

Closed 05000335/2008005-02

URI

Failure of the Automatic Diesel Fuel Oil Transfer

System Could Potentially Result in the 1A EDG Being

Inoperable (4OA5.3)

2

Attachment

05000389/2008-002-00

LER

Unit 2 Manually Tripped as a Result of Maintenance

Activities (4OA3.1)

05000389/2008-003-00

LER

Unit 2 Condensate Pump Failure Resulting in Manual Reactor Trip (4OA3.2)

2515/176

TI

EDG TS Surveillance Requirements Regarding

Endurance and Margin Testing (Section 4OA5.2)

Opened and Closed 05000335/2009002-01

NCV

Failure to Perform a Required TS Surveillance (1R22)05000335/2009002-02

NCV

Failure to Take Timely and Effective Corrective Actions

for EDG Day Tank Level Switch Failure (4OA2.3)05000335/2009002-03

NCV

Failure to Perform an Adequate Post Maintenance Test

on the 1A-EDG Fuel Oil Day Tank Low Level Switch

(4OA5.3)05000389/2009002-04

NCV

Failure to Implement Adequate Process Controls during

Maintenance Activities Resulted in a Manual Reactor Trip (4OA3.1)

LIST OF DOCUMENTS REVIEWED

Procedures

ADM-25.02, NRC Performance Indicators, Rev. 21A

ADM-04.02, Industrial Safety Program, Rev. 11A

ADM-78.01, Post Maintenance Testing, Rev. 30A

1-ARP-06-A16, Annunciator Response Procedure 1A EDG Panel, Revs. 1 & 2

1-OSP-59.11, Simultaneous Start of 1A EDG and 1B EDG Periodic Test, Rev. 1

2-OSP-59.11, Simultaneous Start of 2A EDG and 2B EDG Periodic Test, Rev. 4

1-OSP-59.01A, 1A EDG Monthly Surveillance

1-OSP-59.01B, 1B EDG Monthly Surveillance, Rev. 8A

2-OSP-59.01A, 2A EDG Monthly Surveillance, Rev. 9

2-OSP-59.05A, 2A EDG Air Start Check Valve Quarterly Test, Rev. 1

2-OSP-59.05B, 2B EDG Air Start Check Valve Quarterly Test, Rev. 1

1-OSP-69.14A, ESF - 18 Month Surveillance for EDG Start on SIAS Without LOOP & 24- Hour

Load Run - Train A

HPP-3, High Radiation Areas, Rev. 26A

2-0330020, Unit 2 Turbine Cooling Water System Normal Operation, Rev. 54

2-NOP-03.05, Aligning and Starting SDC Loop 2A, Rev. 40

EP-SR-102-1000, Nuclear Division Florida Alert and Notification System Guideline,

Rev. 0

06.80.02-E, Protection & Control Siren Maintenance Procedure, 01/11/2006

3

Attachment

06.80.01-I, Transmission and Substation Siren System Availability Test Procedure, Rev.

04/03/2008

NPSS-EP-WP-001, Public Alert Notification System Testing, Maintenance, and

Engineering, Rev. 2

EPG-06, Maintenance of the Emergency Recall System, Rev. 0

EPG-04, Drill and Exercise Program, Rev. 4

EPIP-13, Maintaining Emergency Preparedness Radiological Emergency Plan Training,

Rev. 19

EPG-03, Review and Revision of Emergency Preparedness Documents, Rev. 2

EPIP-01, Classification of Emergencies, Rev. 15 and16

EPIP-02, Duties and Responsibilities of the Emergency coordinator, Rev. 26 and 27

EPIP-06, Activation and Operation of the Emergency Operations Facility, Rev. 19 and 20

EPIP-08, Off-site Notifications and Protective Action Recommendations, Rev. 17, 18, 19,

and 19A

PI-AA-204, Condition Identification and Screening Process, Rev. 0

PI-AA-205, Condition Evaluation and Corrective Action, Rev. 0

EP-AA-100-1001, Guidelines for Maintaining Emergency Preparedness, Rev. 0

EP-AA-100-1002, Emergency Preparedness Change Review Committee Guideline,

Rev. 0

ADM-25.02, NRC Performance Indicators, Rev. 21B

EPG-01, Emergency Preparedness Assessment and Performance Monitoring, Rev. 4

Records, Calculations, and Data Reviewed

Work Order 35013863, L-29 Alarm and Power Supply Failure

Work Order 34004771, CEDS Power Supply Replacement

Work Order 37012672, Level Switch for Diesel Oil Day Tank 1A2 Low Level Control

Work Order 38024041, Level Switch for Diesel Oil Day Tank 1A2 Low Level Control

JPN-PSL-SEIP-93-049, EDG Instrument Setpoint Evaluation

PSL-1FSM-09-004, EDG Fuel Oil DOST Gravity Feed St. Lucie 1

Siren System Availability Test Records

Quarterly Siren Maintenance records: 1st and 3rd Quarters 2007

Quarterly Siren Maintenance records: 2nd and 4th Quarters 2008

Siren Extended (Annual) Maintenance records: 2008

St. Lucie Plant Emergency Response Directory, Rev. 51

Data packages for Pager Tests: 1st, 2nd, 3rd, and 4th Quarters 2008

First Quarter Training Drill package, February 15, 2007

Second Quarter Training Drill package, June 21, 2007

First Quarter Training Drill package, January 17, 2008

Second Quarter Training Drill package, April 23, 2008

Third Quarter Training Drill package, August 6, 2008

Fourth Quarter Training Drill package, December 10, 2008

Emergency Plan, Rev. 52, 53 and 54

Documentation of DEP opportunities: 1st, 2nd, 3rd, and 4th Quarters 2008

Drill and exercise participation records of ERO personnel, 1st, 2nd, 3rd, and 4th Quarters

2008

Siren testing data 1st, 2nd, 3rd, and 4th Quarters 2008

4

Attachment

Audits and Self-Assessments

PSL-08-07, Emergency Preparedness Functional Area Audit, August 12 - September 30,

2008

QSL-EP-07-08, Emergency Preparedness Functional Area Audit, August 6 - September

25, 2007

2008-31296, Self Assessment Quick Hit: 2008 EP Drill and Exercise Trends, October 10,

2008

2008-5397, Readiness Review for 2009 NEI 06-04 Hostile Action Based Drill Self-

Assessment, April 17 - September 30, 2008

2007-2668, Self Assessment Drill and Exercise Performance, January 02, 2007

Condition Reports

2008-6080

2008-22556

2008-32722

2008-33187

2009-0047

2009-0068

2009-0083

2009-0295

2009-0430

2009-0864

2009-1448

2009-1844

2009-1955

2009-1958

2009-1991

2009-2190

2009-3627

2009-4088

2009-7255

2009-9414

2007-17693

2008-26171

2008-31884

2008-324418

2009-2238

2009-2256

2009-2304

2009-2311

2009-2390

2009-2402

2009-2513

2009-2603

2009-3054

2009-3075

2009-3133

2009-3278

2009-3756

2009-3894

2009-3897

2009-3911

2007-1115

2007-14893

2007-17768

2007-20283

2007-38527

2009-4456

2009-4542

2009-4548

2009-4650

2009-4659

2009-4671

2009-4731

2009-4754

2009-4839

2009-4976

2009-4989

2009-5022

2009-5031

2009-5181

2009-5186

2007-18295

2007-18347

2007-38527

2008-5674

2008-34978

2009-4004

2009-4053

2009-5334

2009-5341

2009-5347

2009-5388

2009-5539

2009-5641

2009-5828

2009-6164

2009-6202

2009-6442

2009-6666

2009-6817

2009-6967

2007-18305

2007-18313

2008-7048

2008-13896

2008-26494

2008-31689

2009-5997

2009-6013

2009-6144

2009-7025

2009-7271

2009-7368

2009-7437

2009-7501

2009-7563

2009-7733

2009-8028

2009-8167

2009-8252

2009-8314

2009-8508

LIST OF ACRONYMS

ANS

Alert and Notification System (ANS) Testing

DEP

Emergency Response Organization Drill/Exercise Performance

EAL

Emergency Action Level

ERO

Emergency Response Organization

NEI

Nuclear Energy Institute

PI

Performance Indicator

PS

Planning Standard

TI

Temporary Instruction