ML083660204

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IR 05000275-08-008; 05000323-08-008; 11/10/08 - 11/20/08; Diablo Canyon Power Plant: Identification and Resolution of Problems
ML083660204
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 12/30/2008
From: Greg Werner
NRC/RGN-IV/DRS/PSB-2
To: Conway J
Pacific Gas & Electric Co
References
IR-08-008
Download: ML083660204 (34)


See also: IR 05000275/2008008

Text

December 30, 2008

John T. Conway

Senior Vice President & Chief Nuclear Officer

Pacific Gas and Electric Company

P.O. Box 3

Mail Code 104/6/601

Avila Beach, CA 93424

SUBJECT: DIABLO CANYON POWER PLANT - NRC PROBLEM IDENTIFICATION AND

RESOLUTION INSPECTION REPORT 05000275/2008008; 05000323/2008008

Dear Mr. Conway:

On November 20, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed the on-site

portion of a team inspection at your Diablo Canyon Power Plant. The enclosed inspection

report documents the inspection findings, which were discussed on November 20, 2008, with

Mr. K. Peters and other members of your staff during an exit meeting.

This inspection reviewed activities conducted under your license as they relate to the

identification and resolution of problems, compliance with the Commissions rules and

regulations, and the conditions of your operating license. Within these areas, the inspection

involved examination of selected procedures and representative records, observations of

activities, and interviews with personnel. The team also interviewed a representative sample of

personnel regarding the condition of your safety conscious work environment at the Diablo

Canyon Power Plant.

The inspection team reviewed approximately 400 action requests and notifications, associated

apparent cause evaluations and non-conformance reports, and other supporting documentation

to assess the processes for the identification and resolution of problems at Diablo Canyon

Power Plant. Based on these reviews, the team concluded that Diablo Canyon Power Plant had

a generally effective corrective action program. In most cases, problems were identified at an

appropriately low threshold and significant problems were adequately assessed and corrected.

The team determined that the procedures and processes that implemented the various aspects

of the corrective action program had been well established prior to October 1, 2008. However,

these procedures and processes were not consistently followed. The team identified several

samples of corrective actions that were limited in scope and not always carried through to

completion. On October 1, 2008, a new corrective action program was implemented which

similarly established appropriately low thresholds for identifying problems and sufficient

processes for assessing and correcting these problems in a timely manner. However, at the

UNITED STATES

NUCLEAR REGULATORY COMMISSION

R E GI ON I V

612 EAST LAMAR BLVD, SUITE 400

ARLINGTON, TEXAS 76011-4125

Pacific Gas and Electric

- 2 -

time of this inspection, these processes were too new for the team to provide a thorough

evaluation of their effectiveness.

On the basis of the approximately thirty interviews conducted during this inspection,

observations of plant activities, and reviews of the corrective action and employee concerns

programs, the team determined that site personnel were willing to raise safety issues to the

attention of management by at least one of the available methods.

This report documents two NRC-identified findings of very low safety significance (Green). One

of these findings was determined to involve a violation of NRC requirements. However,

because of the very low safety significance and because it is entered into your corrective action

program, the NRC is treating this finding as a non-cited violation (NCV), consistent with Section

VI.A.1 of the NRC Enforcement Policy. If you contest either finding in this report, you should

provide a response within 30 days of the date of this inspection report, with the basis for your

denial, to the U. S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001, with copies to the Regional Administrator, Region IV; the Director,

Office of Enforcement, U. S. Nuclear Regulatory Commission, Washington, DC 20555-0001;

and the NRC Resident Inspector at the Diablo Canyon Power Plant.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response, if any, will be made available electronically for public inspection

in the NRC Public Document Room or from the Publicly Available Records component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Gregory Werner, Chief

Plant Support Branch 2

Division of Reactor Safety

Dockets: 50-275

50-323

Licenses: DPR-80

DPR-82

Enclosure:

NRC Inspection Report 05000275/2008008 and 05000323/2008008

w/Attachments: Supplemental Information, Information Requests

Pacific Gas and Electric

- 3 -

cc w/Enclosure:

Sierra Club San Lucia Chapter

ATTN: Andrew Christie

P. O. Box 15755

San Luis Obispo, CA 93406

Nancy Culver

San Luis Obispo

Mothers for Peace

P. O. Box 164

Pismo Beach, CA 93448

Chairman

San Luis Obispo County

Board of Supervisors

1055 Monterey Street, Suite D430

San Luis Obispo, CA 93408

Truman Burns\\Robert Kinosian

California Public Utilities Commission

505 Van Ness Ave., Rm. 4102

San Francisco, CA 94102

Diablo Canyon Independent Safety Committee

Attn: Robert R. Wellington, Esq.

Legal Counsel

857 Cass Street, Suite D

Monterey, CA 93940

Director, Radiological Health Branch

State Department of Health Services

P. O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414

City Editor

The Tribune

3825 South Higuera Street

P. O. Box 112

San Luis Obispo, CA 93406-0112

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 31)

Sacramento, CA 95814

Pacific Gas and Electric

- 4 -

James R. Becker, Site Vice President &

Station Director

Diablo Canyon Power Plant

P. O. Box 56

Avila Beach, CA 93424

Jennifer Tang

Field Representative

United States Senator Barbara Boxer

1700 Montgomery Street, Suite 240

San Francisco, CA 94111

Chief, Radiological Emergency Preparedness Section

National Preparedness Directorate

Technological Hazards Division

Department of Homeland Security

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Pacific Gas and Electric

- 5 -

Electronic distribution by RIV:

Regional Administrator (Elmo.Collins@nrc.gov)

Deputy Regional Administrator (Chuck.Casto@nrc.gov)

DRP Director (Dwight.Chamberlain@nrc.gov)

DRP Deputy Director (Anton.Vegel@nrc.gov)

DRS Director (Roy.Caniano@nrc.gov)

DRS Deputy Director (Troy.Pruett@nrc.gov)

Senior Resident Inspector (Michael.Peck@nrc.gov)

Resident Inspector (Tony.Brown@nrc.gov)

Branch Chief, DRP/B (Vincent.Gaddy@nrc.gov)

Senior Project Engineer, DRP/B (Rick.Deese@nrc.gov)

DC Site Secretary (Agnes.Chan@nrc.gov)

Public Affairs Officer (Victor.Dricks@nrc.gov)

Team Leader, DRP/TSS (Chuck.Paulk@nrc.gov)

RITS Coordinator (Marisa.Herrera@nrc.gov)

Only inspection reports to the following:

DRS STA (Dale.Powers@nrc.gov)

S. Williams, OEDO RIV Coordinator (Shawn.Williams@nrc.gov)

ROPreports

ML083660204

SUNSI Rev Compl.

x Yes No

ADAMS

x Yes No

Reviewer Initials

GEW

Publicly Avail

x Yes No

Sensitive

Yes x No

Sens. Type Initials

GEW

SRI/PSB2

SRA

RI/PBB

RI/EB2

C/PSB2

EARusch

MFRunyan

MABrown

GPTutak

GEWerner

/RA/

/RA/

/RA/

/RA/

/RA/

12/18/08

12/18/08

12/18/08

12/18/08

12/30/08

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

- 1 -

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets:

50-275, 50-323

Licenses:

DPR-80, DPR-82

Report:

05000275/2008008

05000323/2008008

Licensee:

Pacific Gas and Electric Company

Facility:

Diablo Canyon Power Plant, Units 1 and 2

Location:

7 1/2 miles NW of Avila Beach

Avila Beach, California

Dates:

November 10-20, 2008

Inspectors:

E. Ruesch, Senior Reactor Inspector (Team Lead)

M. Runyan, Senior Reactor Analyst

M. Brown, Resident Inspector

M. Baquera, Reactor Inspector

G. Tutak, Reactor Inspector

Approved By:

G. Werner, Chief

Plant Support Branch 2

Division of Reactor Safety

- 2 -

Enclosure

SUMMARY OF FINDINGS

IR 05000275/2008008; 05000323/2008008; 11/10/08 - 11/20/08; Diablo Canyon Power Plant:

Identification and Resolution of Problems.

This team inspection was performed by a senior reactor inspector, a senior reactor analyst, a

resident inspector, and two region-based reactor inspectors. Two findings of very low safety

significance (Green) were identified during the inspection. One was classified as a non-cited

violation (NCV), the other as a finding. The significance of most findings is indicated by their

color (Green, White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance

Determination Process." Findings for which the significance determination process does not

apply may be Green or be assigned a severity level after NRC managements review. The

NRCs program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG-1649, "Reactor Oversight Process," Revision 4, dated December 2006.

Identification and Resolution of Problems

The inspection team reviewed approximately 400 action requests and notifications, associated

apparent cause evaluations and non-conformance reports, and other supporting documentation

to assess the processes for the identification and resolution of problems at Diablo Canyon

Power Plant. The team also performed a five-year review of the auxiliary feed water system to

determine whether problems were being effectively addressed. Based on these reviews, the

team concluded that Diablo Canyon Power Plant had a generally consistent and effective

corrective action program. In most cases, problems were identified at an appropriately low

threshold and significant problems were adequately assessed and corrected. The team

determined that, with the exception of the process for prioritization of issues, the procedures

and processes that implemented the various aspects of the corrective action program were well

established prior to October 1, 2008. However, these processes were not consistently followed.

The team identified several samples of corrective actions that were limited in scope and not

always carried through to completion. On October 1, 2008, the licensee established a new

corrective action program which likewise established appropriately low thresholds for identifying

problems and established sufficient processes for assessing, prioritizing, and correcting these

problems in a timely manner. However, at the time of this inspection, these processes were too

new for the team to provide a thorough evaluation of their effectiveness.

Overall, the team determined that the licensee had appropriately evaluated industry operating

experience for relevance to the facility and had entered applicable items into the corrective

action program.

Quality assurance audits were generally effective in identifying substantive issues and areas for

improvement. However, several of the actions and recommendations generated from these

audits were not acted on in a timely and thorough manner. Other self-assessment activities

were narrowly focused and often did not identify any insightful issues concerning performance,

limiting the value of the assessments.

On the basis of approximately thirty interviews conducted during and prior to this inspection,

observations of plant activities, and reviews of the corrective action and employee concerns

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Enclosure

programs, the team determined that site personnel were willing to raise safety issues to the

attention of management. While several workers interviewed expressed a reluctance to report

problems to management directly or to document issues in the corrective action program, all

were willing to raise concerns to management attention by at least one of the several methods

available.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Mitigating Systems

Criterion V, Instructions, Procedures, and Drawings, for the failure to properly

implement housekeeping procedures to prevent seismically-induced system

interactions. Specifically, the team identified two instances during a plant walk down

where transient equipment was staged in the vicinity of safety-related equipment

identified as seismically-induced system interaction targets. This transient equipment

had not been analyzed to assess the risk to these safety-related components.

Following identification by the team, licensee staff secured and analyzed the transient

equipment. Licensee staff entered this finding into the corrective action program as

Notifications 50084856 and 50084761.

The failure of plant personnel to follow the requirements to properly secure or analyze

equipment in close proximity to sensitive equipment was a performance deficiency.

The finding was more than minor because it was similar to Inspection Manual Chapter 0612, Power Reactor Inspection Reports Appendix E, Example 3.j., in that it was

indicative of a significant programmatic deficiency in the licensees Seismically-

Induced System Interactions Program that could lead to worse errors if uncorrected.

Specifically, a change in program ownership in 2006 resulted in a degradation of the

sensitivity of plant personnel to the risk of seismically-induced system interactions due

to transient materials, insufficient training of plant personnel on the program, and an

absence of quality records over an approximately two-year period. Using Inspection

Manual Chapter 0609.04, Phase 1 - Initial Screening and Characterization of

Findings, the finding was determined to have very low safety significance because it

did not result in an actual loss of a system safety function, did not result in a loss of a

single train of safety equipment for greater than its technical specification allowed

outage time, did not involve the loss or degradation of equipment specifically

designed to mitigate a seismic, flooding, or severe weather initiating event, and did

not involve the total loss of any safety function that contributes to an external event

initiated core damage accident sequence. This finding has a cross-cutting aspect in

the area of human performance associated with the work practices area component

because the licensee failed to define and effectively communicate expectations

regarding procedural compliance and personnel failed to follow procedures H.4(b)

(Section 4OA2.a.3(a)).

- 4 -

Enclosure

Cornerstone: Public Radiation Safety

  • Green. The team identified a finding for failure to take adequate corrective actions to

correct adverse trends in control of radioactive and potentially contaminated material

as required by the corrective action program. Specifically, between May 2005 and

June 2008, the licensee on two occasions identified and failed to correct adverse

trends in the control of radioactive and potentially contaminated material. Licensee

staff entered this finding into the corrective action program as Notification 50085121.

The finding was more than minor because it affected the Public Radiation Safety

cornerstone objective to ensure adequate protection of public health and safety from

exposure to radioactive materials released into the public domain as a result of

routine civilian nuclear reactor operation. Using Inspection Manual Chapter 0609

Appendix D, Public Radiation Safety Significance Determination Process, the finding

was determined to have very low safety significance because the dose impact to a

member of the public was less than or equal to 0.005 rem total effective dose

equivalent . The finding has a cross-cutting aspect in the area of problem

identification and resolution, associated with the corrective action area component;

because the licensee failed to thoroughly evaluate problems such that the resolution

addressed the cause P.1(c) (Section 4OA2.a.3(b)).

B.

Licensee-Identified Violations

None

- 5 -

Enclosure

REPORT DETAILS

4.

OTHER ACTIVITIES (OA)

4OA2 Problem Identification and Resolution (71152B)

The team based the following conclusions, in part, on a review of issues that were

identified during the assessment period, which ranged from June 15, 2006, (the last

biennial problem identification and resolution inspection) to the end of the on-site portion

of the inspection on November 20, 2008.

.a

Assessment of Corrective Action Program (CAP) Effectiveness

.1

Inspection Scope

The team reviewed a sample of approximately 400 action requests and notifications,

including associated root cause and apparent cause evaluations, from approximately

35,000 that had been initiated between June 2006 and November 2008 to determine if

problems were being properly identified, characterized, and entered into the corrective

action program for evaluation and resolution. The team reviewed work requests and

attended the licensees daily notification review team meeting to assess reporting

thresholds, prioritization efforts, and significance determination processes, and to

observe the corrective action programs interfaces with the operability assessment and

work control processes. The team reviewed root cause and apparent cause evaluations

to verify that the licensee considered the full extent of cause and extent of condition for

problems and to determine how the licensee assessed generic implications and previous

occurrences. The team assessed the timeliness and effectiveness of corrective actions,

completed or planned, and looked for additional examples of similar problems. The

team conducted interviews with plant personnel to identify other processes that may

exist where problems may be identified and addressed outside of the corrective action

program.

The team performed a five-year review of operability evaluations, equipment issues, and

corrective actions associated with the auxiliary feed water system to determine whether

problems were being effectively addressed. The team conducted a walk down of this

system to assess the physical condition of equipment and to determine if problems were

identified and entered into the corrective action process at an appropriate threshold.

During this inspection period, the licensee converted its corrective action program from

its legacy Plant Information Management System (PIMS) to a new software tool called

Systems, Analysis and Programs (SAP). This conversion, which was completed on

October 1, 2008, included the migration of all open action requests from PIMS to SAP;

all closed action requests were archived in the PIMS system. The team performed a

review of the processes used for this conversion and discussed associated procedural

changes with licensee staff.

- 6 -

Enclosure

.2

Assessments

Effectiveness of Problem Identification

The team concluded that most problems were identified and documented in accordance

with the licensees corrective action program guidance and NRC requirements. Based

on the approximately 35,000 action requests and notifications written during the period

and on discussions with licensee personnel, the team concluded that although entry of

issues into the corrective action program was not always accomplished in a timely

manner, licensee staff generally identified problems at an appropriately low threshold.

The team noted three exceptions to this conclusion, two specific and one general:

On October 15, 2007, inspectors identified black soot on the Emergency Diesel

Generator 1-1 exhaust manifold. Licensee personnel subsequently identified that

one of four fasteners connecting the exhaust manifold to the turbo charger was

missing. The soot buildup had been present since the last previous operation of

the diesel generator on September 23, 2007. By procedure, plant operators were

required to perform at least one inspection of the diesel generator each shift, to

maintain awareness of equipment condition, and to report problems in a timely

manner. This failure to identify a degraded condition was documented as non-

cited Violation (NCV) 2007005-01.

During the walk down of the auxiliary feed water system, the team identified two

instances of transient equipment that was neither secured nor analyzed as

required by Procedure AD4.ID3, SISIP Housekeeping Activities, Revision 6

(see 4OA2.a.3(a)). This procedure further requires that any identified

deficiencies be promptly entered into the corrective action program. However,

licensee personnel failed to enter one of the identified deficiencies into the

corrective action program until prompted by the team.

Through discussions and interviews with licensee personnel, the team

determined that some personnel were reluctant to enter problems into the

corrective action program (see 4OA2.d.2). Several personnel stated that the

origination of issues in the corrective action program was the responsibility of

their supervisors. Several others stated that due to their knowledge of improperly

dispositioned issues, they had lost confidence in the corrective action program

and were hesitant to use it to resolve issues. Further, while most of the

interviewees stated that the corrective action program had a low threshold,

almost none knew what the threshold was or where it could be found in plant

procedures.

- 7 -

Enclosure

Effectiveness of Prioritization and Evaluation of Issues

The team determined that while the licensee was identifying most problems at an

appropriately low threshold and that most conditions were assessed and ultimately

corrected, the prioritization of issues within the corrective action program was deficient.

Further, while the procedures and processes that implemented the various aspects of

the corrective action program had been well established prior to October 1, 2008, these

procedures and processes had not always been followed.

Although the licensees legacy corrective action program provided a prioritization

scheme, it was not used. Through interviews with licensee personnel, the team

determined that licensee staff prioritized corrective actions based only on whether the

issue had been identified as a quality problem, not based on the assigned priority. The

determination of whether an issue was a quality problem was made by the Action

Request Review Team during their daily review of action requests. This quality problem

determination did not address safety significance. Until late 2007, these determinations

were made using guidance contained in an uncontrolled document referred to as the

Action Request Review Team Tribal Knowledge Document, which was noted on at

least one occasion to directly conflict with quality-related procedures (Action Request

A0637738). Further, issues were at times prioritized based on actual or potential

regulatory consequences versus safety significance of the issue. Examples included:

The quality problem statement for Action Request A0639139 determined the

associated issue to be a quality problem, stating, NRC non-cited violations

(NCV) and licensee identified violations (LIV) events for 2002 through 2004

indicate a negative trend in violations due to increased numbers of events of the

release of radioactive material from the radiologically controlled area.

The quality problem statement for Action Request A0694780 stated, The ARRT

determined that this issue is a quality problem based on the possibility that

further review by the NRC will result in a green non-cited violation. If the NRC

review determines that the problem is minor and does not warrant a green non-

cited violation, contact a member of the AR Review Team for a re-evaluation of

the quality problem determination.

The quality problem statement for Action Request A0703351 determined the

associated issue to be a quality problem, stating, There is a continuing negative

trend in the NRC violations and plant events regarding the unauthorized release

of radioactive material from the RCA.

On October 1, 2008, the licensee established a new corrective action program that

procedurally established appropriately low thresholds for identifying problems and

sufficient processes for assessing, prioritizing, and correcting these problems in a timely

manner. This program put in place several tools and procedural changes that, if

accompanied by changes in the licensee culture, have the potential to mitigate many of

the prioritization and evaluation problems noted by the team. Further, procedures

associated with the new corrective action program establish better and more objective

- 8 -

Enclosure

guidance on prioritization of issues. The team noted, however, during the observation of

a Notification Review Team meeting, that these new procedures and expectations were

at the time of the inspection still in the process of being implemented; they had not yet

been fully embraced by licensee staff. Overall, these processes were too new for the

team to provide a thorough evaluation of their effectiveness.

Effectiveness of Corrective Actions

While in most cases, problems were being identified at an appropriately low threshold,

assessed, and corrected, the team identified numerous instances of untimely,

inadequate, or ineffective corrective actions. The team noted that in March 2008,

licensee management noted deficiencies in the implementation of the corrective action

program by licensee staff, including the untimely resolution of issues. A root cause

investigation (NCR N0002221) was initiated. During an August 2008 internal audit of the

corrective action program, the licensees quality verification department similarly

concluded that there were deficiencies in corrective action program implementation.

The team determined that the licensees corrective action process, including apparent

cause evaluations, typically addressed issues as isolated instances and that issues were

often not specifically evaluated for their cumulative impact or significance. The team

noted that in many cases, corrective actions for identified issues were unnecessarily

delayed and/or the recommended actions were changed to enable the licensee to meet

timeliness goals. Examples included:

In August 2006, Action Request A0675752 was initiated to address NRC

Information Notice 2006-17, Recent Operating Experience of Service Water

Systems Due to External Conditions. When the licensee attempted to

implement the recommended corrective actions, they were determined to be

inadequate and put on hold. The action request was later closed with no actions

taken. After being identified by the team, this issue was entered into the

licensees corrective action program as Notification 50084672.

In May 2007, Action Request A0696350 was initiated to address NRC

Information Notice 2007-17, Fires at Nuclear Power Plants Involving Inadequate

Fire Protection Administrative and Design Controls. Corrective actions included

making changes to Procedure OM8.ID1, Fire Loss Prevention. The

implementation of these corrective actions, required by procedure to be

accomplished within 180 days, was delayed several times to permit the

development of formal training on the proposed procedural changes. When the

procedural changes were implemented in April 2008, no formal training was

conducted. The action request was closed in May 2008.

In July 2007, as a result of a finding in an internal licensee audit of the radiation

protection program, an apparent cause evaluation (Action Request A0703362)

was initiated to address ineffective and untimely implementation of the corrective

action program by radiation protection personnel. By procedure, this apparent

- 9 -

Enclosure

cause evaluation was required to be completed within 30 days. However, it was

inappropriately delayed and was not completed until March 2008.

In July 2007, as a result of a finding in an internal licensee audit of the radiation

protection program, Action Request A0703351 was initiated to address an

adverse trend in the release of radioactive material from the radiologically

controlled area. The due date of the associated corrective actions was twice

delayed and then closed in June 2008. The team determined that the corrective

actions were inadequate and that the trend was inappropriately closed (see

section 4OA2.a.3(b)).

The team reviewed a sample of condition reports that involved operability issues to

assess the adequacy and timeliness of the operability assessment process. The team

noted several operability review problems including inconsistent or incomplete

engineering evaluations and unverified assumptions. Two NRC-identified NCVs were

issued during the report period for operability-related issues:

On two occasions between September 29 and November 9, 2006, operations

and engineering personnel failed to address operability when using manual

actions in place of automatic actions associated with the auxiliary building

ventilation system (NCV 2006005-02).

Between April 2006 and April 2007, in violation of its operability determination

procedure, the licensee failed to complete a required prompt operability

determination until approximately one year after the immediate operability

determination was performed (NCV 2008003-02).

The team concluded that the licensee had an acceptable root cause determination

process that was adequately implemented. Appropriate corrective actions were

identified to address each cause and operating experience and off-site expertise were

appropriately utilized during these evaluations. However, as previously discussed, these

corrective actions were not always completed as recommended.

.3

Findings

(a) Failure to Identify and Correct Violations of the Seismically-Induced Systems Interaction

Program

Introduction. The team identified a Green non-cited violation of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, for the failure to

properly implement housekeeping procedures to prevent seismically-induced system

interactions as required by the licensees Seismically-Induced Systems Interaction

Program (SISIP), which implements the requirements of Task II.C.3, Systems

Interactions, of NUREG-0660. Specifically, the team identified two instances during a

plant walk down where transient equipment was staged in the vicinity of safety-related

equipment identified as seismically-induced system interaction targets. This transient

equipment had not been analyzed to assess the risk to these safety-related

- 10 -

Enclosure

components. Following identification by the team, licensee staff secured and analyzed

the transient equipment.

Description. On November 12, 2008, the inspectors identified two instances of transient

equipment located in the vicinity of sensitive plant structures, systems, and components

that had been identified in the SISIP as potential targets for seismically-induced system

interactions. Specifically, a wheeled portable radiation monitor was discovered in the

Unit 2 containment penetration room near auxiliary feed water piping and display

stanchions were discovered in the Unit 1 containment penetration room near safety

injection and containment spray system piping. In both cases, the transient equipment

was not secured and had not been evaluated in accordance with Section 5.1.3 of

Procedure AD4.ID3, SISIP Housekeeping Activities. Until asked by the inspectors,

plant personnel failed to enter the identification of the unsecured radiation monitor into

the corrective action program in accordance with Section 5.6 of Procedure AD4.ID3.

Upon further investigation, the inspectors determined that records of SISIP walk downs

had not been maintained since 2006, when ownership of the program was transferred

from the quality verification department to the Housekeeping Department. Section 5.7 of

Procedure AD4.ID3 requires that inspections of all plant areas be performed monthly to

identify and correct situations where there is a potential for system interactions as a

result of a seismic event. Pacific Gas and Electric was unable to provide documentation

demonstrating that these required inspections had been performed.

The inspectors further concluded that no formal qualification and training was provided

for personnel responsible for performing these inspections. Pacific Gas and Electric

relied upon the instructions of Procedure AD4.ID3 to provide training. No training was

provided to plant personnel on the importance of recognizing and identifying potential

seismically-induced system interaction hazards.

Analysis. The failure of plant personnel to follow the requirements to properly secure or

analyze equipment in close proximity to sensitive equipment was a performance

deficiency. The finding was more than minor because it was similar to Inspection

Manual Chapter 0612, Power Reactor Inspection Reports, Appendix E, Example 3.j., in

that it was indicative of a significant programmatic deficiency in the licensees

Seismically-Induced System Interactions Program that could lead to worse errors if

uncorrected. Specifically, a change in program ownership in 2006 resulted in a

degradation of the sensitivity of plant personnel to the risk of seismically-induced system

interactions due to transient materials, insufficient training of plant personnel on the

program, and an absence of quality records over an approximately two-year period.

Using Inspection Manual Chapter 0609.04, Phase 1 - Initial Screening and

Characterization of Findings, the finding was determined to have very low safety

significance because it did not result in an actual loss of a system safety function, did not

result in a loss of a single train of safety equipment for greater than its technical

specification allowed outage time, did not involve the loss or degradation of equipment

specifically designed to mitigate a seismic, flooding, or severe weather initiating event,

and did not involve the total loss of any safety function that contributes to an external

event initiated core damage accident sequence. This finding has a cross-cutting aspect

- 11 -

Enclosure

in the area of human performance associated with the work practices area component

because the licensee failed to define and effectively communicate expectations

regarding procedural compliance and personnel failed to follow procedures H.4(b).

Enforcement. 10 CFR Part 50, Appendix B, Criterion V, "Instructions, Procedures, and

Drawings," requires that activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings, of a type appropriate to the circumstances and

shall be accomplished in accordance with these instructions, procedures, or drawings.

Instructions, procedures, or drawings shall include appropriate quantitative or qualitative

acceptance criteria for determining that important activities have been satisfactorily

accomplished. Procedure AD4.ID3, SISIP Housekeeping Activities, Section 5.1.3

requires that transient equipment located near safety-related equipment be secured, set

back, or evaluated. Contrary to the above, on November 12, 2008, the inspectors

identified transient equipment located near safety-related equipment that was not

secured, set back, or evaluated. Because this finding was of very low safety significance

and was entered into the licensees corrective action program as Notifications 50084856

and 50084761, this violation is being treated as an NCV, consistent with Section VI.A of

the Enforcement Policy: NCV 05000275;05000323/2008008-01; Failure to Identify and

Correct Violations of the Seismically-Induced Systems Interaction Program.

(b) Failure to take appropriate actions to correct an identified adverse trend

Introduction. The team identified a Green finding for failure to take adequate corrective

actions to correct adverse trends in control of radioactive and potentially contaminated

material as required by the licensees corrective action program. Specifically, between

May 2005 and June 2008, the licensee on two occasions identified and failed to correct

adverse trends in the control of radioactive and potentially contaminated material.

Description. In May 2005, a routine audit of the radiation protection program by the

licensees quality verification department identified an adverse trend in the release of

radioactive material from the radiologically controlled area. The audit identified sixteen

events during the two-year audit period, two of which resulted in the issuance of Green

non-cited violations.

During a subsequent routine audit in 2007, the licensees quality verification department

again identified a negative trend in radioactive material controls. During this second

audit period there were seven radioactive material control events, one of which resulted

in a Green non-cited violation. The 2007 audit identified that corrective actions

associated with the non-cited violation issued during that audit period were too narrowly

scoped and that other corrective actions were untimely. Twenty-nine findings were

entered into the corrective action program as a result of this audit. These included (1) a

finding of a continued adverse trend in the control of radioactive material and (2) a

finding of ineffective implementation of the corrective action program by radiation

protection personnel (Action Requests A0703351 and A0703362, respectively).

Action Request A0703351 was initiated on July 18, 2007, with four corrective actions

recommended, including a review of previous apparent causes and corrective actions to

- 12 -

Enclosure

determine what was effective and sustainable. On August 1, 2007, the due date for

these corrective actions was extended to February 17, 2008. On October 25, 2007, the

due date was changed to December 31, 2007. On December 31, 2007, the due date

was again extended to June 30, 2008. On June 30, 2008, the action request was closed

with two of the four corrective actions taken. No review of previous apparent causes and

corrective actions was documented. The basis for closure stated, No events in the last

six months. No finding for RP program audit completed June 08. However, the

inspectors identified two events which occurred between January 2008 and June 2008.

Specifically:

On April 5, 2008, four purple-painted tools containing fixed contamination were

found in a drum of clean tools outside the radiologically controlled area. This

was documented in Action Request A0726562.

On April 12, 2008, Action Request A0723504 documented a purple-painted tool

found outside of the radiologically controlled area. While this tool was later

surveyed and found to be free of contamination, the licensees radiation

protection department uses purple paint to mark contaminated tools and

routinely handles all purple-painted tools as contaminated. Similar instances

were documented as contributors to the previously identified adverse trends.

The inspectors determined that these events were indicative of a continued adverse

trend. Further, in September 2008, the licensee again noted an adverse trend in

radioactive material control, identifying seven events (Action Request A0741786).

However, this trend did not identify that a similar trend was inappropriately closed out

three months prior.

Analysis. The failure of Pacific Gas and Electric to follow the requirements of its

corrective action program was a performance deficiency. The finding was more than

minor because it affected the Public Radiation Safety cornerstone objective to ensure

adequate protection of public health and safety from exposure to radioactive materials

released into the public domain as a result of routine civilian nuclear reactor operation.

The inspectors assessed the significance of this finding using Inspection Manual

Chapter 0609 Appendix D, Public Radiation Safety Significance Determination

Process. The inspectors concluded that this finding was of very low safety significance

because the dose impact to a member of the public was less than or equal to 0.005 rem

total effective dose equivalent (TEDE). The finding has a cross-cutting aspect in the

area of problem identification and resolution, associated with the corrective action area

component; because the licensee failed to thoroughly evaluate problems such that the

resolution addressed the cause P.1(c).

Enforcement. Licensee Procedure OM7, Corrective Action Program, requires, in part,

that the licensee evaluate problems commensurate with their significance, determine

their cause, and conduct a proper evaluation and resolution of repeat occurrences. The

procedure further requires that corrective actions are completed in a timely manner

consistent with the problem significance. The licensee did not meet this meet this self-

imposed standard, in that, between May 2005 and June 2008, plant personnel twice

- 13 -

Enclosure

identified and failed to properly evaluate and resolve adverse trends in the control of

radioactive and potentially contaminated materials. The licensee entered this finding

into the corrective action program as Notification 50085121. Because this performance

deficiency does not involve a violation of regulatory requirements, enforcement action

does not apply: Finding (FIN) 05000275;05000323/2008008-02, Failure to Take

Appropriate Actions to Correct an Identified Adverse Trend.

.b

Assessment of the Use of Operating Experience

.1

Inspection Scope

The team examined the licensee's program for reviewing industry operating experience,

including reviewing the governing procedure and evaluating self-assessments. The

team reviewed a sample of operating experience notification documents that had been

issued during the assessment period to determine whether the licensee had

appropriately evaluated the notification for relevance to the facility. The team also

examined whether the licensee had entered those items into the corrective action

program and assigned actions to address the issues. The team reviewed a sample of

root cause evaluations and significant condition reports to verify that the licensee had

appropriately included industry operating experience.

.2

Assessment

Overall, the team determined that the licensee had appropriately evaluated industry

operating experience for relevance to the facility, and had entered applicable items in the

corrective action program. Once evaluated, assessments of the issues were generally

appropriate. The team also determined that the licensee was evaluating industry

operating experience when performing root cause and apparent cause evaluations.

.3

Findings

No findings of significance were identified.

.c

Assessment of Self-Assessments and Audits

.1

Inspection Scope

The team reviewed a sample of licensee self-assessments and audits to assess whether

the licensee was regularly identifying performance trends and effectively addressing

them. The team also reviewed audit reports to determine the effectiveness of

assessments in specific areas.

.2

Assessment

The team determined that audits conducted during the inspection period by the

licensees quality verification department were thorough and critical, identifying several

opportunities for improvement of the assessed programs. However, many of the issues

- 14 -

Enclosure

identified in these audits were not acted upon in a timely manner. The licensees

corrective action program required that apparent cause evaluations be performed within

thirty days on all audit findings. The team noted several examples where items were not

completed in a timely manner (some of these examples are noted in Section 4OA2.a.2).

The team further identified that during the inspection period the quality verification

department, responsible for performing a majority of the audits and self-assessments

experienced a disproportionately high level of personnel turnover. Specifically, in the

eighteen months prior to this inspection, the department lost ten experienced

employees. These losses were the result of layoffs and the unexpected departure of

several individuals. In addition, there were two changes in the department directorship

over the same period. The team determined that these personnel losses and

management changes resulted in insufficient resources to complete all tasks in a high-

quality manner. The team did not identify any indication of unfulfilled regulatory

commitments as a result of these changes, but the capability to conduct key activities

and effective independent audit assessment was adversely impacted.

The team noted that in March 2008, a self-assessment by licensee management

resulted in the initiation of a root cause investigation to address noted deficiencies in the

corrective action program (Non-Conformance Report N0002221). As a result of items

identified in this root cause investigation, the licensee has generated an Integrated

Action Plan to improve corrective action performance.

.3

Findings

No findings of significance were identified.

.d

Assessment of Safety Conscious Work Environment

.1

Inspection Scope

The team conducted focused interviews with 30 individuals from plant operations,

electrical maintenance, and engineering, including supervisory and non-supervisory

personnel, to assess whether conditions exist which would challenge the establishment

of a safety conscious work environment at Diablo Canyon Power Plant. The team

conducted additional interviews with quality assurance personnel and the manager

responsible for the employee concerns program.

- 15 -

Enclosure

.2

Assessment

There are several vehicles established through which employees and contractors may

raise concerns to management. In addition to the ability to raise a concern directly to a

supervisor or to the NRC, formal programs included the corrective action program, the

employee concerns program, and the differing professional opinion program. While all

interviewees were willing to raise safety concerns through at least one of the available

methods, the team concluded that some plant personnel were hesitant to raise concerns

via one or more of these avenues. Examples included:

Several interviewees provided examples where specific station managers did not

appropriately respond to concerns raised during planning meetings. Some

interviewees felt this behavior resulted in the hesitance of other plant personnel

to bring issues up at these meetings.

Several interviewees discussed examples of negative comments and/or body

language at operations turnover meetings after safety issues were raised.

More senior operators generally felt that a chilling affect occurred as a result of

the disposition of a specific personnel issue in the 1990s. Some plant operations

personnel stated that this chilled affect caused a continued barrier to the vigorous

pursuit of safety issues within the operations organization.

Plant personnel generally felt that the corrective action program was effective. Several

interviewees provided examples of issues improperly dispositioned by the corrective

action program. These examples, which included prioritization and timeliness of

corrective actions and ineffective corrective actions, resulted in some personnel losing

confidence in the corrective action program and becoming hesitant to use the program to

resolve issues. While most of the interviewees stated the corrective action program had

a low threshold, almost none of the personnel interviewed knew what this threshold was

or where the threshold could be found in plant procedures.

About half of those interviewed exhibited a good understanding of the employee

concerns program. While several plant operators and one engineer expressed strongly

negative feelings about the effectiveness of the employee concerns program and its

methods for maintaining confidentiality, only one interviewee was aware of an example

of a perceived breach of confidentiality within the program. The employee concerns

program categorized concerns as either nuclear safety/quality issues or as other

issues. The team noted that all of the nuclear safety/quality issues for the past two and

a half years were explicitly related to NRC-referred allegations; the program treated non-

nuclear safety/quality issues informally.

Most interviewees stated that they had received training on safety conscious work

environment. However, only three interviewees were able to correctly describe the

attributes of a safety conscious work environment. Most interviewees associated safety

conscious work environment with various industrial safety programs.

- 16 -

Enclosure

Very few interviewees were familiar with the differing professional opinion process. The

inspectors reviewed the single differing professional opinion file maintained in the

employee concerns program files and concluded that the differing professional opinion

was processed in accordance with station procedures. The team concluded that this

differing professional opinion indirectly resulted in an adverse affect on the willingness

within a particular engineering organization to raise concerns due to the related increase

in workload.

The team concluded that site personnel were willing to raise safety issues to the

attention of management. While several workers interviewed expressed a reluctance to

report problems to management directly or to document issues in the corrective action

program, all were willing to raise concerns to management attention by at least one of

the several methods available.

.3

Findings

No findings of significance were identified.

4OA6 Management Meetings

Exit Meeting

On October 20, 2008, the preliminary results of the inspection were discussed with

Mr. Peters and other members of the licensee staff. The licensee confirmed that no

proprietary information was handled during this inspection.

Attachments:

1. Supplemental Information

2. Information Request (May 14, 2008)

3. Information Request (October 14, 2008)

A-1

Attachment 1

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

H. Garcia, Engineer, Design Engineering

R. Glines, Auditor, Quality Verification

R. Gray, Engineer, Radiation Protection

W. Guldemond, Director, Site Services

J. Hodges, Project Quality Supervisor, Quality Verification

L. Hopson, Manager, Problem Prevention & Resolution

T. Juarez, Engineer, Mechanical Systems Engineering

S. Ketelsen, Manager, Regulatory Services

G. Lautt, Plant Quality Assurance Supervisor, Quality Verification

A. Maple, Process Improvement Coordinator, Engineering

M. McCoy, Senior Engineer, Regulatory Services

K. Millenaar, Intern, Regulatory Services

C. Over, Corrective Action Program Supervisor, Problem Prevention & Resolution

K. Peters, Station Director

M. Somerville, Manager, Radiation Protection

B. Waltos, Programs Supervisor, Technical Support Engineering

S. Zawalick, Senior Engineer, Regulatory Services

NRC

L. Carson, Senior Health Physicist, Plant Support Branch 2

M. Peck, Senior Resident Inspector, Diablo Canyon

D. Proulx, Senior Project Engineer, Reactor Projects Branch D

G. Werner, Chief, Plant Support Branch 2, Division of Reactor Safety

A-2

Attachment 1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

05000275;05000323/2008008-01

NCV

Failure to Identify and Correct Violations of the

Seismically Induced Systems Interaction Program

05000275;05000323/2008008-02

FIN

Failure to Take Appropriate Actions to Correct an

Identified Adverse Trend

A-3

Attachment 1

LIST OF DOCUMENTS REVIEWED

Action Requests:

A0067824

A0644594

A0676729

A0695972

A0715625

A0732001

A0125170

A0648578

A0677707

A0696297

A0715672

A0732266

A0196253

A0648581

A0677755

A0696350

A0715758

A0732643

A0331690

A0649158

A0678338

A0696953

A0715782

A0732836

A0406114

A0650104

A0678429

A0698528

A0716109

A0732976

A0408506

A0650216

A0678535

A0699162

A0716235

A0733673

A0519389

A0650404

A0678658

A0699496

A0717009

A0733674

A0545551

A0652122

A0678820

A0699655

A0717066

A0733675

A0550724

A0652663

A0679347

A0700176

A0717645

A0733679

A0552602

A0652882

A0679381

A0700190

A0717715

A0733681

A0555585

A0653879

A0679382

A0700231

A0718292

A0733682

A0557136

A0655264

A0679395

A0700559

A0718533

A0733683

A0558200

A0656196

A0679734

A0700663

A0718946

A0733685

A0558721

A0657132

A0679979

A0700745

A0719361

A0733686

A0560365

A0658595

A0680025

A0700864

A0719494

A0733687

A0565195

A0658846

A0680722

A0700892

A0719500

A0733689

A0565847

A0659068

A0681148

A0701328

A0719585

A0733690

A0569316

A0659091

A0681464

A0701791

A0719596

A0733693

A0571619

A0659407

A0682398

A0701835

A0719774

A0733694

A0574318

A0660589

A0682690

A0702236

A0719901

A0733695

A0574698

A0661022

A0683293

A0702276

A0720218

A0733697

A0576754

A0661997

A0683360

A0702304

A0720552

A0733698

A0577093

A0662373

A0683442

A0702816

A0721437

A0733699

A0577098

A0662699

A0683475

A0702845

A0721949

A0733700

A0577100

A0662902

A0683727

A0703224

A0722689

A0733701

A0577295

A0663496

A0684192

A0703244

A0723281

A0733702

A0577522

A0663823

A0684202

A0703351

A0723331

A0733703

A0579843

A0663923

A0684385

A0704318

A0723373

A0733704

A0581305

A0664992

A0684572

A0704824

A0723504

A0733729

A0584931

A0665039

A0684631

A0704871

A0723606

A0734529

A0587537

A0665101

A0685069

A0705303

A0724266

A0734535

A0590309

A0665153

A0685161

A0706450

A0724748

A0734536

A0593262

A0665166

A0685775

A0706704

A0724816

A0734830

A0595257

A0665501

A0686244

A0706980

A0725004

A0735113

A0595263

A0665588

A0686674

A0707628

A0725081

A0736063

A0595672

A0666110

A0686794

A0708019

A0725381

A0736228

A0597712

A0666414

A0687009

A0708447

A0725835

A0737235

A0598779

A0666980

A0688061

A0709237

A0725933

A0737237

A0603677

A0666983

A0688202

A0709399

A0726218

A0737959

A-4

Attachment 1

A0613008

A0666984

A0688735

A0709407

A0726408

A0738064

A0613109

A0666985

A0688992

A0710059

A0726562

A0738079

A0613505

A0666990

A0689527

A0710082

A0726774

A0738260

A0614168

A0668929

A0690266

A0710187

A0727113

A0738268

A0615476

A0669226

A0690634

A0710328

A0727573

A0738519

A0617328

A0669468

A0691337

A0710335

A0727949

A0738964

A0620857

A0672242

A0691366

A0710868

A0728599

A0739136

A0623594

A0672417

A0691464

A0711318

A0728908

A0739307

A0625556

A0672419

A0691477

A0711645

A0729286

A0739505

A0626496

A0672422

A0691736

A0712328

A0729807

A0741297

A0630009

A0673108

A0692370

A0712329

A0730171

A0741409

A0630537

A0673125

A0692689

A0712539

A0730246

A0741456

A0635271

A0675254

A0692739

A0712803

A0730658

A0741786

A0635392

A0675603

A0692962

A0713307

A0730749

A0741803

A0637471

A0675752

A0693042

A0713616

A0730876

A0639139

A0676321

A0693300

A0713859

A0731551

A0640802

A0676400

A0695538

A0713960

A0731731

A0641000

A0676595

A0695960

A0715336

A0731961

Notifications:

50032470

50037116

50039994

50040530

50044120

50084761

50032491

50038369

50040043

50040531

50044121

50084848

50032543

50039696

50040515

50040532

50044214

50084849

50032648

50039697

50040519

50041762

50044215

50084911

50032683

50039708

50040521

50043354

50044216

50084991

50032779

50039710

50040522

50043760

50044217

50085430

50032791

50039712

50040523

50043976

50044218

50085545

50032794

50039713

50040524

50044097

50044219

50032846

50039716

50040525

50044098

50070591

50032874

50039768

50040526

50044105

50078086

50032990

50039783

50040528

50044116

50084648

Orders:

60005500

A-5

Attachment 1

Non-Conformance Reports (Root Cause Evaluations):

N0002175

N0002209

N0002213

N0002218

N0002222

N0002227

N0002200

N0002210

N0002214

N0002219

N0002223

N0002201

N0002211

N0002215

N0002220

N0002224

N0002203

N0002212

N0002216

N0002221

N0002226

Licensee Event Reports

LER 2008-001

Procedures:

Human Error Investigation Tool, Revision 1

2R14 Maintenance Activities Assessment Checklist M.11, Housekeeping and Material Condition

2T15 Maintenance Activities Assessment Checklist M.11, Housekeeping and Material Condition

AD4.DC2, Plant Material Condition and Housekeeping, Revision 9

AD4.ID1, Housekeeping, Revision 10

AD4.ID2, Plant leakage Evaluation, Revision 6A

AD4.ID2, Plant leakage Evaluation, Revision 7

AD4.ID2, Plant leakage Evaluation, Revision 8

AD4.ID3, SISIP Housekeeping Activities, Revision 6

AD7.ID2, Standard Plant Priority Assignment Scheme, Revision 10

AD7.ID4, On-Line Maintenance Scheduling, Revision 12

AD7.ID8, Project Management, Revision 1

AWP SP-003, Oversight and Alignment of SGT CAP with the DCPP CAP, Revision 0

CF3.ID9, Design Change Development, Revision 32

CF4.ID3, Modification Implementation, Revision 21

ECG 18.7, Fire Rated Assemblies, Revision 6

ER1.ID2, Boric Acid Control Program, Revision 1

ER1.ID2, Boric Acid Control Program, Revision 2

M-1106, Auxiliary Feedwater Pump Room Flooding, Revision 0

M-49919, Elimination of Floor Drain Credit from HELB/MELB Design Basis Flooding Analysis,

Revision 0

MA1.ID14, Plant Crane Operating Restrictions, Revision 17

A-6

Attachment 1

OM15.ID1, Human Performance Program, Revision 2

OM4.ID17, Project Review Committee, Revision 1

OM4.ID17, Project Review Committee, Revision 4

OM4.ID3, Assessment of Industry Operating Experience, Revision 13

OM7.ID1, Problem Identification and Resolution, Revision 27

OM7.ID1, Problem Identification and Resolution, Revision 28

OM7.ID11, 10 CFR 21 Reportability Review Process, Revision 2

OM7.ID4, Root Cause Analysis and Apparent Cause Evaluations, Revision 11

OM8.ID1, Fire Loss Prevention, Revision 19

Operations Policy C-1, Plant Power Level Official Indication, Revision 12

OPJ-6B:IV, Manual Operation of DG 1-1, Revision 27

RCP D-614, Release of Solid Materials from Radiologically Controlled Areas, Revision 14

STP I-7-M.1, RCS Wide Range Pressure and RVLIS Transmitters Calibration, Revision 4

STP M-70C, Inspection/Maintenance of Doors, Revision 15

STP M-9A, Diesel Engine Generator Routine Surveillance Test, Revision 78

STP P-AFW-A11, Comprehensive Testing of Turbine-Driven Auxiliary Feedwater Pump 1-1,

Revision 2

STP P-AFW-A11, Comprehensive Testing of Turbine-Driven Auxiliary Feedwater Pump 1-1,

Revision 3

STP P-AFW-A21, Comprehensive Pump Test for Turbine-Driven Auxiliary Feedwater Pump 2-

1, Revision 1A

STP P-AFW-A21, Comprehensive Pump Test for Turbine-Driven Auxiliary Feedwater Pump 2-

1, Revision 2

STP R-22, Thimble Tube Inspection, Revision 9

TP TA-0701, Work Control Process During PIMS Unavailability, Revision 1A

TQ2.ID4, Training Program Implementation, Revision 15

Drawings:

DC-663056-31-1, Motor-Driven Auxiliary Feedwater Pump Curves, April 13, 1971

106703, Sheet 3, Auxiliary Feedwater System, Revision 71

106704, Sheet 3, Auxiliary Feedwater Pump 1-1, Revision 88

102032, Sheet 27 Page 0, Rev. 101

102009, Sheet 3 Page 0, Rev. 62

A-7

Attachment 1

57731, Equipment Location Section D-D Containment Turbine and Fuel Handling Buildings,

Change 11

57729, Mechanical, Equipment Location Section B-B, Auxiliary and Containment Buildings,

Revision 14

57725, Mechanical, Equipment Location, Plan and Elevation 91-0 & 100-0 Aux., Containment

and Fuel Handling Bldgs, Revision 29

Audits and Assessments:

Audit #0881290001, 2008 Corrective Action Program Audit

Audit #071290004, 2007 Radiation Protection Program Audit

Plant Performance Improvement Report, October 2008

Quality Verification Short Form Assessment #080990011, April 10, 2008

SGT Corrective Action Program Audit, September 24, 2007

Quality Verification Short Form Assessment #072620010, September 19, 2007

Seismically Induced System Interaction Program Self-Assessment Report, November 2003

2005 Quality Performance Assessment Report

2007 Diablo Canyon Power Plant Quality Assurance Program and Procedures Audit

Quality Verification Department Bi-weekly Observation Report, January 2008

Quality Verification Department Bi-weekly Observation Report, March 2008

Quality Verification Department Bi-weekly Observation Report, April 2008

Assessment No. 032680010

Assessment No. 081290001

Nuclear Industry Evaluation Program (NIEP) of the Diablo Canyon Power Plant Quality

Organization, July 28, 2008

Other:

(a)(1) Goal Setting Summary Report, dated 11/17/2008

ARRT Action Request Review Guidance, Revision 32

Auxiliary Feedwater Maintenance Rule Unavailability Line Chart, November 19, 2008

Auxiliary Feedwater System Health Report, November 19, 2008

DCM S-25A

DCM S-9

DCM T-24

A-8

Attachment 1

DCPP AR Backlog at Tech Down, September 24, 2008

Diablo Canyon Power Plant Health Issue 2008-S069-002, Start Up Voltage improvement for

DCPP power block distribution,

Diablo Canyon Power Plant List of Employees Qualified as Cause Analysts, November 18, 2008

Diablo Canyon Units 1 & 2 EQ File IH06 ASCO Catalog NP Solenoid Valves, Revision 18

Information Notice No. 84-23, Results of the NRC-Sponsored Research Test on ASCO

Solenoid Valves, April 5, 1984

Information Notice No. 88-24, Failure of Air Operated Valves Affecting Safety Related

Systems, May 13, 1988

Maintenance Rule (a)(1) Goal Setting Summary Report, November 17, 2008

Plant Health Improvement Project List, November 18, 2008

Seismically Induced System Interaction Manual, Revision 9

System 3B, Auxiliary Feedwater System, Maintenance Rule Scoping Determination, Revision 3

System 9, Safety Injection, Maintenance Rule Scoping Determination, Revision 3

Vendor Manual, ASCO Valves, DC 663190, Sheet 68, Rev. 3

Notifications generated as a result of this inspection:

50084648

Oil drips below the MDAFW pump

50084672

Flush of AFW suction piping not evaluated

50084729

Open/Closed indication on vlv MU-1-297 and -298

50084761

Stanchions in U1 GE Pen Room - SISI

50084856

Gooseneck air monitor in U2 GE Pen Room - SISI

50084948

Evaluate potential for future placement of equipment without appropriate

SISI consideration

50084959

Documentation of SISI walkdowns

50084975

Notification not written for air sampler SISI issue

50084991

ASCO solenoid valve problem history/evaluation

50085119

Effectiveness of QV audit of SGRP

50085121

Effectiveness of CAs to prevent release of RAM

50085133

SISIP inspection training gaps

50085134

Quality record driving qual tracking

50085393

SISIP implementation weakness

50085527

Vendor manual info as OE?

50037116

AFW room floor drain MR scoping

A-1

Attachment 2

Information Request

May14, 2008

Diablo Canyon Problem Identification and Resolution Inspection

(IP 71152; Inspection Report 05000275; 323/2008008)

The inspection will cover issues addressed during the period of June 15, 2006 through May 15,

2008, but will include a 5-year review of the Auxiliary Feedwater System. All requested

information should be limited to this period unless otherwise specified. The information may be

provided in either electronic or paper media or a combination of these. Information provided in

electronic media may be in the form of e-mail attachment(s), CDs, thumb drives, or 3 2 inch

floppy disks. The agency=s text editing software is MS Word; can also support Excel, Power

Point, and Adobe Acrobat (.pdf) text files. In lieu of hard copies, the information may be placed

on the Certrec website (IMS).

Please provide the following information to David Proulx (dlp@NRC.gov) by May 23, 2008:

Note: On summary lists please include a description of problem, status, initiating date, and

owner organization.

1.

Summary list of all action requests of significant conditions adverse to quality opened or

closed during the period. This includes a summary list of all QEs and NCRs.

2.

Summary list of all action requests (non-RT) which were generated during the period.

3.

A list of all corrective action documents that subsume or "roll-up" one or more smaller

issues for the period

4.

Summary list of all action requests which were down-graded or up-graded in

significance, or were cancelled during the period.

5.

List of all root cause analyses completed during the period.

6.

List of root cause analyses planned, but not complete at end of the period.

7.

List of all apparent cause analyses completed during the period.

8.

List of plant safety issues raised or addressed by the employee concerns program

during the period (Employee Concerns Program log).

9.

List of action items generated or addressed by the plant safety review committees during

the period

10.

All quality assurance audits and surveillances of corrective action activities completed

during the period.

11.

A list of all quality assurance audits and surveillances scheduled for completion during

the period, but which were not completed.

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Attachment 2

12.

All corrective action activity reports, functional area self-assessments, and non-NRC

third party assessments completed during the period.

13.

Corrective action performance trending/tracking information generated during the period

and broken down by functional organization

14.

Current revisions of corrective action program procedures. This includes initiation,

evaluation and corrective actions, processing root and apparent cause evaluations,

operability assessments, extent of cause/condition reviews, quality assurance program

procedures, operational experience, employee concerns/differing professional opinions,

and procedures for implementing a safety conscious work environment.

15.

A listing of all external events evaluated for applicability at Diablo Canyon during the

assessment period.

16.

Action requests or other actions generated for each of the items below issued during the

assessment period:

Part 21 Reports

Applicable NRC Information Notices

All LERs issued by Pacific Gas and Electric during the period

NCVs and Violations issued to PG&E during the period (including licensee

identified violations).

17.

Safeguards event logs for the period

18.

Radiation protection event logs

19.

Current system health reports or similar information for the AFW System

20.

Current predictive performance summary reports or similar information for the AFW

system

21.

Corrective action effectiveness review reports generated during the period

22.

List of risk significant components and systems (ranked by importance measures).

23.

List of ARs, NCRs and QEs on the AFW system from June 15, 2003 to May 15, 2008.

24.

Current design basis documents and system drawings for the AFW system.

25.

Plant Organizational Charts (both management and working level).

A-1

Attachment 3

Information Request

October 14, 2008

Diablo Canyon Problem Identification and Resolution Inspection

(IP 71152; Inspection Report 05000275; 323/2008008)

The inspection will cover issues addressed during the period of June 15, 2006 through October

15, 2008, but will include a 5-year review of the Auxiliary Feedwater System. All requested

information should be limited to this period unless otherwise specified. The information may be

provided in either electronic or paper media or a combination of these. Information provided in

electronic media may be in the form of e-mail attachment(s), CDs, thumb drives, or 3 2 inch

floppy disks. The agency=s text editing software is MS Word; can also support Excel, Power

Point, and Adobe Acrobat (.pdf) text files. In lieu of hard copies, the information may be placed

on the Certrec website (IMS).

This information request was originally sent on May 14, 2008, covering the period from June 15,

2006, through May 15, 2008. In responding to this request, please include only new information

not provided in your last response.

Please provide the following information to Eric Ruesch (eric.ruesch@nrc.gov) by October 20,

2008:

Note: On summary lists please include a description of problem, status, initiating date, and

owner organization.

17.

Summary list of all action requests of significant conditions adverse to quality opened or

closed during the period. This includes a summary list of all QEs and NCRs.

18.

Summary list of all action requests (non-RT) which were generated during the period.

19.

A list of all corrective action documents that subsume or "roll-up" one or more smaller

issues for the period

20.

Summary list of all action requests which were down-graded or up-graded in

significance, or were cancelled during the period.

21.

List of all root cause analyses completed during the period.

22.

List of root cause analyses planned, but not complete at end of the period.

23.

List of all apparent cause analyses completed during the period.

24.

List of plant safety issues raised or addressed by the employee concerns program

during the period (Employee Concerns Program log).

25.

List of action items generated or addressed by the plant safety review committees during

the period

A-2

Attachment 3

26.

All quality assurance audits and surveillances of corrective action activities completed

during the period.

27.

A list of all quality assurance audits and surveillances scheduled for completion during

the period, but which were not completed.

28.

All corrective action activity reports, functional area self-assessments, and non-NRC

third party assessments completed during the period.

29.

Corrective action performance trending/tracking information generated during the period

and broken down by functional organization

30.

Current revisions of corrective action program procedures. This includes initiation,

evaluation and corrective actions, processing root and apparent cause evaluations,

operability assessments, extent of cause/condition reviews, quality assurance program

procedures, operational experience, employee concerns/differing professional opinions,

and procedures for implementing a safety conscious work environment.

31.

A listing of all external events evaluated for applicability at Diablo Canyon during the

assessment period.

32.

Action requests or other actions generated for each of the items below issued during the

assessment period:

Part 21 Reports

Applicable NRC Information Notices

All LERs issued by Pacific Gas and Electric during the period

NCVs and Violations issued to PG&E during the period (including licensee

identified violations).

17.

Safeguards event logs for the period

18.

Radiation protection event logs

19.

Current system health reports or similar information for the AFW System

20.

Current predictive performance summary reports or similar information for the AFW

system

21.

Corrective action effectiveness review reports generated during the period

22.

List of risk significant components and systems (ranked by importance measures).

23.

List of ARs, NCRs and QEs on the AFW system from June 15, 2003 to May 15, 2008.

A-3

Attachment 3

24.

Current design basis documents and system drawings for the AFW system.

25.

Plant Organizational Charts (both management and working level).