ML053110530

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IR 05000313-05-004, IR 05000368-05-004 on 06/24/2005 - 09/23/2005; Arkansas Nuclear One, Units 1 and 2; Maintenance Risk Assessments, Operator Performance During Nonroutine Plant Evolutions and Events, Problem Identification and Resolution
ML053110530
Person / Time
Site: Arkansas Nuclear  Entergy icon.png
Issue date: 11/07/2005
From: Graves D
NRC/RGN-IV/DRP/RPB-E
To: Forbes J
Entergy Operations
References
IR-05-004
Download: ML053110530 (47)


See also: IR 05000313/2005004

Text

November 7, 2005

Jeffrey S. Forbes, Vice President,

Operations

Arkansas Nuclear One

Entergy Operations, Inc.

1448 S.R. 333

Russellville, Arkansas 72801-0967

SUBJECT: ARKANSAS NUCLEAR ONE - NRC INTEGRATED INSPECTION REPORT

05000313/2005004 AND 05000368/2005004

Dear Mr. Forbes:

On September 23, 2005, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Arkansas Nuclear One, Units 1 and 2, facility. The enclosed integrated

report documents the inspection findings, which were discussed on September 28, 2005, with

you and other members of your staff.

The inspection examined activities conducted under your licenses as they relate to safety and

compliance with the Commission's rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

The report documents five inspector identified and self-revealing findings of very low safety

significance (Green). Three of these findings were determined to involve violations of NRC

requirements; however, because the findings were entered into your corrective action program,

the NRC is treating these violations as noncited violations consistent with Section VI.A of the

Enforcement Policy. Additionally, a licensee identified violation which was determined to be of

very low safety significance is listed in this report. If you contest these noncited violations, you

should provide a response within 30 days of the date of this inspection report, with the basis for

your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington DC 20555-0001; with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas

76011-4005; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission,

Washington DC 20555-0001; and the NRC Resident Inspector at Arkansas Nuclear One,

Units 1 and 2, facility.

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be made available electronically for public inspection

Entergy Operations, Inc.

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in the NRC Public Document Room or from the Publicly Available Records (PARS) component

of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

David N. Graves, Chief

Project Branch E

Division of Reactor Projects

Dockets: 50-313

50-368

Licenses: DPR-51

NPF-6

Enclosure:

NRC Inspection Report 05000313/2005004 and 05000368/2005004

w/Attachment: Supplemental Information and Phase 3 Evaluation, Damaged Reactor Coolant

Pump Seal, Arkansas Nuclear One, Unit 2

cc w/enclosure:

Senior Vice President

& Chief Operating Officer

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Vice President

Operations Support

Entergy Operations, Inc.

P.O. Box 31995

Jackson, MS 39286-1995

Manager, Washington Nuclear Operations

ABB Combustion Engineering Nuclear

Power

12300 Twinbrook Parkway, Suite 330

Rockville, MD 20852

County Judge of Pope County

Pope County Courthouse

100 West Main Street

Russellville, AR 72801

Entergy Operations, Inc.

-3-

Winston & Strawn LLP

1700 K Street, N.W.

Washington, DC 20006-3817

Bernard Bevill

Radiation Control Team Leader

Division of Radiation Control and

Emergency Management

Arkansas Department of Health

4815 West Markham Street, Mail Slot 30

Little Rock, AR 72205-3867

James Mallay

Director, Regulatory Affairs

Framatome ANP

3815 Old Forest Road

Lynchburg, VA 24501

Technological Services Branch

Chief

FEMA Region VI

800 North Loop 288

Federal Regional Center

Denton, Texas 76201-3698

Entergy Operations, Inc.

-4-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (RWD)

Branch Chief, DRP/E (DNG)

Senior Project Engineer, DRP/E (VGG)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

Regional State Liaison Officer (WAM)

NRR/DIPM/EPB/EPHP (REK)

DRS STA (DAP)

J. Dixon-Herrity, OEDO RIV Coordinator (JLD)

ROPreports

ANO Site Secretary (VLH)

SISP Review Completed: DNG ADAMS: / Yes G No Initials: _DNG_____

/ Publicly Available G Non-Publicly Available

G Sensitive / Non-Sensitive

R:\\_ANO\\2005\\AN2005-04RP-RWD.wpd

RIV:RI:DRP/E

RI:DRP/E

SRI:DRP/E

C:DRS/PSB

JLDixon

ELCrowe

RWDeese

MPShannon

VGGaddy for

VGGaddy for

VGGaddy for

/RA/

11/02/05

11/02/05

11/02/05

10/31/05

C:DRS/OB

C:DRS/EMB

C:DRS/PEB

C:DRP/E

TGody

CJPaulk

LJSmith

DNGraves

/RA/

/RA/

/RA/

/RA/

11/01/05

11/01/05

11/02/05

11/07/05

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets:

50-313, 50-368

Licenses:

DPR-51, NPF-6

Report:

05000313/2005004 and 05000368/2005004

Licensee:

Entergy Operations, Inc.

Facility:

Arkansas Nuclear One, Units 1 and 2

Location:

Junction of Hwy. 64W and Hwy. 333 South

Russellville, Arkansas

Dates:

June 24 through September 23, 2005

Inspectors:

K. Clayton, Operations Engineer

E. Crowe, Resident Inspector

R. Deese, Senior Resident Inspector

J. Dixon, Resident Inspector

P. Elkmann, Emergency Preparedness Inspector

P. Goldberg, Reactor Inspector

W. McNeill, Reactor Inspector

M. Murphy, Senior Operations Engineer

Approved By:

David N. Graves, Chief, Project Branch E

Division of Reactor Projects

Enclosure

CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -1-

1R01

Adverse Weather Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -1-

1R04

Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -2-

1R05

Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -2-

1R06

Flood Protection Measures . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -4-

1RO7 Heat Sink Performance . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -5-

1R11

Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . -6-

1R12

Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -7-

1R13

Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . -8-

1R14

Operator Performance During Nonroutine Plant Evolutions and Events . . . -11-

1R15

Operability Evaluations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -14-

1R16

Operator Workarounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -14-

1R17

Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -15-

1R19

Postmaintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -15-

1R22

Surveillance Testing

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -16-

1R23

Temporary Plant Modifications

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -17-

1EP2 Alert Notification System Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -18-

1EP3 Emergency Response Organization Augmentation Testing (71114.03) . . . -18-

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies . . . -19-

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -19-

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -20-

4OA2 Problem Identification and Resolution . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -21-

4OA3 Event Followup . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -24-

4OA4 Crosscutting Aspects of Findings

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -24-

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -25-

4OA6 Meetings, Including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -26-

4OA7 Licensee-Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . -26-

ATTACHMENT 1: . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . A-2

LIST OF DOCUMENTS REVIEWED . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-3

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-12

ATTACHMENT 2: PHASE 3 EVALUATION, DAMAGED REACTOR COOLANT PUMP SEAL

ARKANSAS NUCLEAR ONE, UNIT 2

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A2-1

Enclosure

SUMMARY OF FINDINGS

IR 05000313/2005004, 05000368/2005004; 6/24/05 - 9/23/05; Arkansas Nuclear One, Units 1

and 2; Maintenance Risk Assessments, Operator Performance During Nonroutine Plant

Evolutions and Events, Problem Identification and Resolution, Other Activities.

This report covered a 3-month period of inspection by resident inspectors and regional

specialist inspectors. Five Green findings, three of which were noncited violations. The

significance of most findings is indicated by their color (Green, White, Yellow, or Red) using

Inspection Manual Chapter 0609, "Significance Determination Process." Findings for which the

significance determination process does not apply may be Green or be assigned a severity

level after NRC management's review. The NRCs program for overseeing the safe operation

of commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight

Process," Revision 3, dated July 2000.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The inspectors reviewed a self-revealing finding for an inadequate

troubleshooting procedure for the Unit 2 pressurizer level instrumentation. When

implemented, the procedure resulted in the unplanned energizing of all

pressurizer heaters with Unit 2 operating at normal operating pressure and a

subsequent increase in reactor coolant system pressure which was not

anticipated by operators. The licensee entered the procedural failure to address

the effect of de-energizing Alarm Relay Bistable 2LC-4627-1BN on the

pressurizer heater circuitry into their corrective action program for resolution.

The cause of the finding is related to the crosscutting element of human

performance.

This finding is greater than minor because it affected the procedure quality

attribute under the initiating events cornerstone objective of limiting the likelihood

of those events that upset plant stability. Using the significance determination

process, the finding was determined to have very low safety significance

because this transient initiator did not contribute to both the likelihood of a

reactor trip and the likelihood that mitigation equipment or functions would not be

available (Section 1R14.1).

Green. The inspectors reviewed a self-revealing finding for an inadequate

maintenance procedure which resulted in Control Element Assembly 50 dropping

into the core with Unit 2 operating at 100 percent rated thermal power. During

troubleshooting efforts for a missing phase on the upper gripper for Control

Element Assembly 56, power to the only gripper holding Control Element

Assembly 50 fully withdrawn (the lower gripper) was removed by instrumentation

and control technicians. The procedure failed to contain detailed guidance to

ensure that Control Element Assembly 50 was properly being held by the upper

gripper. The licensee performed a thorough root cause of the event to

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Enclosure

determine the short and long term corrective actions. The cause of the finding is

related to the crosscutting element of human performance.

This finding is greater than minor because it affected the procedure quality

attribute under the initiating events cornerstone objective of limiting those events

that upset plant stability. Using the significance determination process, the

finding was determined to have very low safety significance because this

transient initiator did not contribute to both the likelihood of a reactor trip and the

likelihood that mitigation equipment or functions would not be available

(Section 1R14).

Cornerstone: Mitigating Systems

Green. The inspectors identified a noncited violation of 10 CFR 50.65(a)(4) for

the failure to perform an adequate risk assessment before replacement activities

associated with Unit 1 decay heat room Cooler VUC-1D. Because the work

procedure referenced an outdated engineering report, it did not include adequate

information to ensure that the required risk management actions were taken.

Mechanical maintenance personnel failed to inform operations personnel that a

Unit 1 decay heat vault door was open and incapable of being readily shut. The

licensee entered this performance deficiency into their corrective action program

for resolution. The cause of the finding is related to the crosscutting element of

human performance.

This finding is more than minor because it affected the attribute under the

mitigating systems cornerstone objective of ensuring the availability of systems

that respond to initiating events to prevent undesirable consequences, in that the

licensee failed to implement compensatory risk management measures. Using

the maintenance risk assessment and risk management significance

determination process, the finding was determined to have very low safety

significance because the performance deficiency was associated only with

inadequate risk management actions and the incremental increase in core

damage probability was negligible (Section 1R13).

Green. The inspectors identified a noncited violation of 10 CFR 50.65(a)(4) for

the failure to perform an adequate risk assessment before the isolation of the

Unit 1 electromatic relief valve. Operators considered that there would be no

impact on plant risk before isolating the electromatic relief valve, but they failed

to consider the increased probability of a pressurizer code safety valve failing to

reseat. The licensee entered this performance deficiency into their corrective

action program for resolution. The cause of the finding is related to the

crosscutting element of human performance.

This finding is greater than minor because it related to a risk assessment which

failed to consider a risk significant component that was unavailable during

maintenance and contained known errors that had the potential to change the

outcome of the assessment. Using the Maintenance Risk Assessment and Risk

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Enclosure

Management Significance determination process, the finding was determined to

have very low safety significance because the inadequate risk assessment only

had an incremental increase in core damage probability of less than 1 x 10-6

(Section 1R13).

Green. The inspectors reviewed a self-revealing noncited violation of Unit 2

Technical Specification 6.4.1, "Procedures," when reactor coolant pump seal

injection flow was established with the reactor coolant pump uncoupled from its

motor. This activity led to damage of the seal for Reactor Coolant

Pump 2P-32C. This damage required conducting an additional reduced reactor

coolant system inventory maintenance period to replace the seal. The licensee

performed a thorough root cause of the event to determine the short and long

term corrective actions. The cause of the finding is related to the crosscutting

element of human performance.

This finding is greater than minor because it affected the procedural quality

attribute under the mitigating systems cornerstone objective of ensuring the

availability and reliability of the reactor coolant system inventory, such that the

licensee had to enter a higher risk plant operating state to repair the seal. Using

the shutdown operations significance determination process, the inspectors

determined the finding required a Phase 2 analysis. In the Phase 2 analysis, risk

analysts determined the finding to be of very low safety significance because

(1) the seal replacement activity only required establishing reduced inventory

conditions (not midloop) and (2) the time needed to replace the seal was not

extensive (Section 4OA5).

Cornerstone: Barrier Integrity

B.

Licensee-Identified Violations

Violations of very low safety significance which were identified by the licensee have

been reviewed by the inspectors. Corrective actions taken or planned by the licensee

have been entered into the licensee's corrective action program. These violations and

their corrective actions are listed in Section 4OA7 of this report.

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period at 100 percent rated thermal power and remained there

throughout the inspection period.

Unit 2 began the inspection period at 100 percent rated thermal power and remained there until

September 8, 2005, when the unit down powered to approximately 65 percent rated thermal

power as a result of a dropped control element assembly (CEA). The unit subsequently

returned to 100 percent rated thermal power on September 10, 2005, and remain there for the

rest of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01

Adverse Weather Protection (71111.01)

a.

Inspection Scope

Readiness for Seasonal Susceptibilities. The inspectors completed a review of the

licensee's readiness of seasonal susceptibilities involving extreme high temperatures.

The inspectors: (1) reviewed plant procedures, the Updated Safety Analysis Report,

and Technical Specifications to ensure that operator actions defined in adverse weather

procedures maintained the readiness of essential systems; (2) walked down portions of

the systems listed below to ensure that adverse weather protection features were

sufficient to support operability including the ability to perform safe shutdown functions;

(3) evaluated operator staffing levels to ensure the licensee would maintain the

readiness of essential systems required by plant procedures; and (4) reviewed the

corrective action program (CAP) to determine if the licensee identified and corrected

problems related to adverse weather conditions.

August 10, 2005, Unit 1 high pressure injection (HPI) and emergency

feedwater (EFW) systems

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

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Enclosure

1R04

Equipment Alignment (71111.04)

a.

Inspection Scope

Partial System Walkdowns. The inspectors: (1) walked down portions of the three risk

important systems listed below and reviewed plant procedures and documents to verify

that critical portions of the selected systems were correctly aligned and (2) compared

deficiencies identified during the walkdown to the licensee's CAP to ensure problems

were being identified and corrected.

August 4, 2005, Unit 1 HPI system

August 10, 2005, Unit 1 EFW system

August 22-23, 2005, Unit 1 safety-related DC electrical system

The inspectors completed three samples.

Complete Walkdown. The inspectors: (1) reviewed plant procedures, drawings, the

Updated Safety Analysis Report, Technical Specifications, and vendor manuals to

determine the correct alignment of the system; (2) reviewed outstanding design issues,

operator work arounds, and CAP documents to determine if open issues affected the

functionality of the system; and (3) verified that the licensee was identifying and

resolving equipment alignment problems.

July 27-29, 2005, Unit 2 containment spray system

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

1R05

Fire Protection (71111.05)

a.

Inspection Scope

Routine Inspection. The inspectors walked down the seven plant areas listed below to

assess the material condition of active and passive fire protection features, their

operational lineup, and their operational effectiveness. The inspectors: (1) verified that

transient combustibles and hot work activities were controlled in accordance with plant

procedures; (2) observed the condition of fire detection devices to verify they remained

functional; (3) observed fire suppression systems to verify they remained functional;

(4) verified that fire extinguishers and hose stations were provided at their designated

locations and that they were in a satisfactory condition; (5) verified that passive fire

protection features (electrical raceway barriers, fire doors, fire dampers, steel fire

proofing, penetration seals, and oil collection systems) were in a satisfactory material

condition; (6) verified that adequate compensatory measures were established for

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Enclosure

degraded or inoperable fire protection features; and (7) reviewed the CAP to determine

if the licensee identified and corrected fire protection problems.

June 30, 2005, Unit 1 Fire Zone 38-Y, EFW pump room

July 12, 2005, Unit 1 Fire Zone 97-R, integrated control system (ICS) relay room

and cable spreading room

July 15, 2005, Unit 2 Fire Zone 2101-AA, north switchgear room

July 19, 2005, Unit 2 Fire Zone 2096-M, motor control center room

July 29, 2005, Unit 1 Fire Zone Area N, intake structure

July 29, 2005, Unit 1 Fire Zone 112-I, lower north electrical penetration room

August 31, 2005, Unit 1 Fire Zone 98-J, emergency diesel generator corridor

b.

Findings

Unit 1 EFW Pump Room Sprinklers

The inspectors identified an unresolved item (URI) for the Unit 1 EFW pump room fire

sprinklers. On June 30, 2005, the inspectors reviewed the licensees commitment for

train separation in Fire Zone 38-Y, Unit 1 EFW pump room. The inspectors learned that

since the licensee could not demonstrate train separation per 10 CFR Part 50,

Appendix R,Section III.G.2, for the as-built configuration, the licensee requested an

exemption from Appendix R in 1988. The exemption was required because the

turbine-driven and motor-driven EFW pumps and cables share a common room and

have as little as 4 feet of electrical separation. One of the requirements from the

granted exemption was that a fire sprinkler system be built and designed per National

Fire Protection Association (NFPA) 15, 1985 Edition, around the turbine-driven

EFW pump. NFPA 15, defined a water spray system as a normally open sprinkler head.

However, upon inspection of Fire Zone 38-Y, the EFW pump room, the inspectors

noticed that the licensees installed sprinkler system had frangible bulb sprinkler heads

installed. The inspectors then reviewed the licensees design change package that

installed the sprinkler system and discovered it stated that the system was designed and

installed using the guidelines of NFPA 13 and 15, 1985 Edition. The licensee could not

provide to the inspectors supporting documentation to show that the installed sprinkler

system met NFPA 15, 1985 Edition, or that a deviation to the NFPA code was

established due to the sprinkler heads being frangible bulb type. The licensee

contracted an NFPA code expert to determine the status of the installed sprinkler

system with regard to the requirements of NFPA 15, 1985 Edition, and is awaiting the

completion of the report. In response to this issue, the licensee established alternate

suppression and hourly fire watch compensatory measures ensuring an on-going safety

concern did not exist. The licensee entered this condition into their CAP as Condition

Report (CR) ANO-1-2005-0954. Pending completion and review of the licensees code

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Enclosure

compliance document and a review of the safety significance by the regional senior

reactor analyst, this finding is considered unresolved (URI 05000313/2005004-01,

"Failure to Comply with Licensing Basis for Emergency Feedwater Pump Room Fire

Sprinklers.")

Unit 1 ICS Relay Room Sprinklers

On July 12, 2005, in preparation for inspection of the ICS relay room, the inspectors

referenced the applicable section of "Arkansas Nuclear One - Units 1 and 2 Fire

Hazards Analysis," Revision 9. The inspectors determined from this review that the

ICS relay room was contained within Fire Zone 97-R which was to be protected by an

automatic deluge suppression system. The inspectors then conducted their walkdown

and noted that no sprinkler systems were in the ICS relay room. The inspectors

questioned licensee fire protection engineers who could not readily explain the

discrepancy and, subsequently, generated CR ANO-1-2005-1158 to explore the

discrepancy. Because the corrective action to explain this discrepancy was still

incomplete, the inspectors identified this condition as a URI 05000313/2005004-02,

"Absence of ICS Relay Room Fire Sprinklers."

1R06

Flood Protection Measures (71111.06)

a.

Inspection Scope

Annual External Flooding. For the building listed below, the inspectors: (1) reviewed

the Updated Safety Analysis Report, the flooding analysis, and plant procedures to

assess seasonal susceptibilities involving external flooding; (2) reviewed the CAP to

determine if the licensee identified and corrected flooding problems; (3) inspected

underground bunkers/manholes to verify the adequacy of: (a) sump pumps, (b) level

alarm circuits, (c) cable splices subject to submergence, and (d) drainage for

bunkers/manholes; (4) verified that operator actions for coping with flooding can

reasonably achieve the desired outcomes; and (5) walked down the areas listed below

to verify the adequacy of (a) equipment seals located below the floodline, (b) floor and

wall penetration seals, (c) watertight door seals, (d) common drain lines and sumps,

(e) sump pumps, level alarms, and control circuits, and (f) temporary or removable flood

barriers.

C

August 29, 2005, Unit 2 auxiliary building

The inspectors completed one sample.

Semiannual Internal Flooding. For the area listed below, the inspectors: (1) reviewed

the Updated Safety Analysis Report, the flooding analysis, and plant procedures to

assess seasonal susceptibilities involving internal flooding; (2) reviewed the CAP to

determine if the licensee identified and corrected flooding problems; (3) inspected

underground bunkers/manholes to verify the adequacy of (a) sump pumps; (b) level

alarm circuits; (c) cable splices subject to submergence; and (d) drainage for

bunkers/manholes; (4) verified that operator actions for coping with flooding can

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Enclosure

reasonably achieve the desired outcomes; and (5) walked down the areas listed below

to verify the adequacy of: (a) equipment seals located below the floodline, (b) floor and

wall penetration seals; (c) watertight door seals; (d) common drain lines and sumps;

(e) sump pumps, level alarms, and control circuits; and (f) temporary or removable flood

barriers.

C

July 27-29, 2005, Unit 2 Train B high pressure safety injection (HPSI), low

pressure safety injection, and containment spray pump room and gallery

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

1RO7 Heat Sink Performance (71111.07)

a.

Inspection Scope

Biennial Inspection. The inspectors reviewed design documents (e.g., calculations and

performance specifications), program documents, implementing documents (e.g., test

and maintenance procedures), and corrective action documents. The inspectors

discussed various corrective action items, heat exchanger testing and cleaning, and

design verification with licensee personnel.

For heat exchangers directly connected to the safety-related service water system, the

inspectors verified whether thermal performance testing, or heat exchanger inspection,

maintenance and cleaning, and the chemistry monitoring program provided sufficient

controls to ensure proper heat transfer. Specifically, the inspectors reviewed: (1) heat

exchanger test methods and test results from performance testing, (2) heat exchanger

inspection and cleaning methods and results, (3) chemical water treatment and results,

and (4) verification of design including flow balancing to ensure sufficient heat

exchanger flow.

For heat exchangers directly or indirectly connected to the safety-related service water

system, the inspectors verified the: (1) condition and operation were consistent with

design assumptions in the heat transfer calculations, (2) potential for water hammer, as

applicable, (3) chemistry controls for heat exchangers indirectly connected to the

safety-related service water system, and (4) redundant and infrequently used heat

exchangers are flow tested periodically to ensure sufficient flow.

If available, the inspectors reviewed additional nondestructive examination results for

the selected heat exchangers that demonstrated structural integrity.

The inspectors selected heat exchangers that ranked high in the plant specific risk

assessment and were directly or indirectly connected to the safety-related service water

system. The inspectors selected the following heat exchangers:

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Enclosure

Unit 1 shutdown cooling heat exchanger

Unit 1 reactor building coolers

Unit 2 engineered safety feature room coolers

The inspectors selected and completed three heat exchanger samples, which meets the

inspection procedure requirement of two to three samples.

The inspectors verified that the licensee had entered significant heat exchanger/heat

sink problems into the CAP. The inspectors reviewed 11 corrective action documents.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification Program (71111.11)

a.

Inspection Scope

Quarterly Inspection. On August 9, 2005, the inspectors observed testing and training

of Unit 1 senior reactor operators and reactor operators to identify deficiencies and

discrepancies in the training, to assess operator performance, and to assess the

evaluator's critique. Training Scenario A1SPGLOR060101, "New OTSGs," Revision 0,

was used and involved a main steam line break inside containment concurrent with an

EFW malfunction which led to overcooling of the reactor coolant system. The main

steam line break was modeled using the once-through SGs which are scheduled for

installation in the upcoming refueling outage.

The inspectors completed one sample.

Biennial Inspection for Unit 1 and Annual Inspection for Unit 2. The inspectors:

(1) evaluated examination security measures and procedures for compliance with

10 CFR 55.49; (2) evaluated the licensees sample plan of the written examinations for

compliance with 10 CFR 55.59 and NUREG-1021, "Operator Licensing Examiner

Standards," as referenced in the facility requalification program procedures; and

(3) evaluated maintenance of license conditions for compliance with 10 CFR 55.53 by

review of facility records (medical and administrative), procedures, and tracking systems

for licensed operator training, qualification, and watchstanding. In addition, the

inspectors reviewed remedial training for examination failures for compliance with facility

procedures and responsiveness to address failed areas.

Furthermore, the inspectors: (1) interviewed six personnel (two operators, two

instructors, the training supervisor, and one evaluator) regarding the policies and

practices for administering examinations, (2) observed the administration of two

dynamic simulator scenarios to one requalification crew; and (3) observed four

evaluators administer six job performance measures, four in the control room simulator

in a dynamic mode and two in the plant under simulated conditions.

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Enclosure

The inspectors also reviewed the remediation process and the results of the biennial

written examination. The results of the examinations were assessed to determine the

licensees appraisal of operator performance and the feedback of performance analysis

to the requalification training program. The inspectors interviewed members of the

training department and operating crews to assess the responsiveness of the licensed

operator requalification program. The inspectors also observed the examination

security maintenance for the operating tests during the examination week.

Additionally, the inspectors assessed the Arkansas Nuclear One, Unit 1,

plant-referenced simulator for compliance with 10 CFR 55.46 using Inspection

Procedure 71111.11 (Section 03.11). This assessment included the adequacy of the

licensees simulation facility for use in operator licensing examinations and for satisfying

experience requirements as prescribed by 10 CFR 55.46. The inspectors reviewed a

sample of simulator performance test records (transient tests, surveillance tests,

malfunction tests, and scenario-based tests), simulator discrepancy report records, and

processes for ensuring simulator fidelity commensurate with 10 CFR 55.46. The

inspectors also interviewed members of the licensees simulator configuration control

group as part of this review.

In addition to the biennial review for Unit 1, the inspectors reviewed the test results of

the Unit 2 annual operating examination for 2005. Since this was the first half of the

biennial requalification testing cycle, the licensee had not yet administered the written

examination. These results were assessed to determine if they were consistent with

NUREG-1021 guidance and Manual Chapter (MC) 0609, Appendix I, "Operator

Requalification Human Performance Significance Determination Process,"

requirements. This review included examination test results for 56 licensed individuals.

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

1R12

Maintenance Effectiveness (71111.12)

a.

Inspection Scope

The inspectors reviewed the two maintenance activities listed below to: (1) verify the

appropriate handling of structure, system, and component (SSC) performance or

condition problems; (2) verify the appropriate handling of degraded SSC functional

performance; (3) evaluate the role of work practices and common cause problems; and

(4) evaluate the handling of SSC issues reviewed under the requirements of the

Maintenance Rule, 10 CFR Part 50, Appendix B, and Technical Specifications.

September 21, 2005, Units 1 and 2 control room emergency ventilation system

inoperabilities

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Enclosure

September 23, 2005, Unit 2 HPSI pump performance

The inspectors completed two samples.

b.

Findings

No findings of significance were identified.

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

Risk Assessment and Management of Risk. The inspectors reviewed the assessment

activities listed below to verify: (1) performance of risk assessments when required by

10 CFR 50.65 (a)(4) and licensee procedures prior to changes in plant configuration for

maintenance activities and plant operations; (2) the accuracy, adequacy, and

completeness of the information considered in the risk assessment; (3) that the licensee

recognizes, and/or enters as applicable, the appropriate licensee-established risk

category according to the risk assessment results and licensee procedures;

and (4) that the licensee identified and corrected problems related to maintenance risk

assessments.

June 13-16, 2005, Unit 2 steam bypass Valve 2CV-0306 and planned

maintenance during the week

June 23, 2005, Unit 1 decay heat room Cooler VUC-1D replacement and

planned maintenance during the week

August 1-5, 2005, Unit 1 HPI Pump P-36A overhaul and planned maintenance

during the week

July 6 through September 23, 2005, Units 1 and 2 preparations inside the

protected area for the Unit 1 replacement outage

The inspectors completed four samples.

Emergent Work Control. The inspectors: (1) verified that the licensee performed

actions to minimize the probability of initiating events and maintained the functional

capability of mitigating systems and barrier integrity systems; (2) verified that emergent

work-related activities such as troubleshooting, work planning/scheduling, establishing

plant conditions, aligning equipment, tagging, temporary modifications, and equipment

restoration did not place the plant in an unacceptable configuration; (3) reviewed the

CAP to determine if the licensee identified and corrected risk assessment and emergent

work control problems.

July 8, 2005, Unit 1 condenser vacuum Pump C-5A inoperability

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Enclosure

August 25, 2005, Unit 1 isolation of the pressurizer electromatic relief

valve (ERV)

The inspectors completed two samples.

b.

Findings

Unit 1 Decay Heat Room Cooler Maintenance

Introduction. The inspectors identified a Green noncited violation (NCV) of

10 CFR 50.65(a)(4) for the failure to perform an adequate risk assessment before the

replacement of Unit 1 decay heat room Cooler VUC-1D.

Description. On June 23, 2005, during the decay heat room Cooler VUC-1D

replacement activities, the licensee opened the Green Train decay heat vault door,

Door 5, to allow for the old cooler to be rigged out of the room. The inspectors noted

that Door 5 was a high energy line break (HELB), fire, and flooding door and then

questioned operators about the status of the equipment in the room and what risk

management actions were being performed as a result of Door 5 being blocked open.

Operations personnel were not aware that the door was blocked open. The inspectors

learned that Maintenance personnel had failed to ensure that Operations personnel had

been informed that they opened Door 5 to remove the old room cooler.

Upon further review, the licensee discovered that the work order package for the job

was outdated and incomplete. The work order package was initially written in 2001 and

referenced an engineering request (ER) which had been superceded since the time the

work order package was written. As a result, the operational impact concerns were out

of date and the appropriate notification points to inform and/or request permission from

operations was not included. The superceded ER that was referenced only addressed

the door from a HELB perspective. Had the licensees up-to-date ER been referenced,

fire and flooding concerns, in addition to HELB concerns, would have been addressed.

The inspectors concluded that as a result of using an outdated work order and a

superceded ER, operations did not ensure that the required risk management actions

were taken, specifically, controls to ensure the establishment of a firewatch and

ensuring that flood mitigation hatches remained closed.

Analysis. The inspectors determined that the failure to ensure proper risk management

actions were taken was a performance deficiency. This finding is greater than minor

because it affected the availability objective of the equipment performance attribute

under the mitigating systems cornerstone, in that, the finding related to the licensee

failing to implement and effectively manage compensatory measures. Using

Appendix K, "Maintenance Risk Assessment and Risk Management Significance

Determination Process," of MC 0609, "Significance Determination Process," the finding

was determined to have very low safety significance (Green) because the performance

deficiency was associated only with inadequate risk management actions and the

incremental increase in core damage probability was negligible (less than 1 x 10-6). This

issue had human performance crosscutting aspects associated with having an

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Enclosure

inadequate work package and maintenance personnel not communicating with

operations personnel which resulted in risk management actions not being

implemented.

Enforcement. 10 CFR 50.65(a)(4) requires, in part, that the licensee shall assess and

manage the increase in risk that may result from proposed maintenance activities.

Contrary to this, on June 23, 2005, the licensee did not adequately assess risk from

maintenance activities that resulted in a HELB, fire, and flooding door being open and

incapable of being readily shut. Because of the very low safety significance and

because the licensee included this condition in the CAP as CR ANO-C-2005-1205, this

violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 05000313/2005004-03, "Failure to Adequately Assess Risk

for a Blocked Decay Heat Vault Door."

Unit 1 ERV Isolation

Introduction. The inspectors identified a Green NCV of 10 CFR 50.65(a)(4) for the

failure to perform an adequate risk assessment associated with the manual isolation of

the Unit 1 ERV.

Description. On August 25, 2005, Unit 1 operators noticed that the acoustic monitor

indication for the Unit 1 pressurizer ERV was not operable. Operators decided to isolate

the ERV by shutting its isolation Valve CV-1000 since the ERV was considered to be

inoperable with its acoustic monitoring indication out of service. Discussions among

operations personnel concluded that the licensee's risk management assessment

program modeled both opened and closed failure modes. They reasoned that since the

ERV was isolated, it could not fail to reseat and that failure mode should not be

accounted for in a risk assessment. The operators also reasoned that, since the valve

was inoperable because of an indication issue, the valve was available and that failure

mode should not be accounted for in the risk assessment model either. As a result, the

operators assumed no impact on risk would be made when isolating the ERV.

The inspectors reviewed the licensee's assessment for the existing plant conditions and

concluded that the licensee had correctly used their risk management program to

assess the risk with the ongoing maintenance with HPI Pump P-36A, low pressure

injection Valve CV-1429, and Inverter Y-25. The inspectors then discovered in the

licensees risk assessment program that fault trees existed which showed that with the

ERV isolated, the pressurizer code safety valves would be the method of preventing

reactor coolant system overpressure since they would open first on any fast breaking

pressure increase transient. Additionally, the inspectors learned that the probability that

the pressurizer code safety valves would not close after lifting would be increased since

their probability of opening increased. From this the inspectors concluded that the

licensees risk assessment was incomplete since it did not incorporate the added risk

from the increased likelihood that a pressurizer code safety valve would stick open.

Analysis. The inspectors considered that the failure to account for the risk of an isolated

ERV was a performance deficiency. The inspectors determined this finding was greater

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Enclosure

than minor because it related to a licensees risk assessment which had known errors

that had the potential to change the outcome of the assessment. Using Appendix K,

"Maintenance Risk Assessment and Risk Management Significance Determination

Process," of MC 0609, "Significance Determination Process," the finding was

determined to have very low safety significance (Green) because the incremental

increase in core damage probability was less than 2.24 X 10-8. In this determination, the

inspectors assumed Inverter Y-25 and HPI Pump P-36A were already out of service for

maintenance when the ERV was isolated. Also, the inspectors used 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> (between

6:59 a.m. and 3:04 p.m. on August 25, 2005) as the time of the inaccurate risk

assessment, which was the time when both the ERV was isolated and Green Train of

the low pressure injection system was removed from service. This issue had human

performance crosscutting aspects associated with operations personnel incorrectly

assuming a component had no risk significance which resulted in a non-conservative

risk assessment.

Enforcement. 10 CFR 50.65(a)(4) requires, in part, that the licensee shall assess and

manage the increase in risk that may result from proposed maintenance activities.

Contrary to this, the licensee did not adequately assess risk from isolating the Unit 1

pressurizer ERV. Because of the very low safety significance and because the licensee

included this condition in the CAP as CR ANO-C-2005-1257, this violation is being

treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000313/2005004-04, "Failure to Adequately Assess Risk for an Isolated

Pressurizer Electromatic Relief Valve."

1R14

Operator Performance During Nonroutine Plant Evolutions and Events (71111.14

and 71153)

a.

Inspection Scope

The inspectors: (1) reviewed operator logs, plant computer data, and/or strip charts for

the evolutions listed below to evaluate operator performance in coping with nonroutine

events and transients; (2) verified that the operator response was in accordance with the

response required by plant procedures and training; and (3) verified that the licensee

has identified and implemented appropriate corrective actions associated with personnel

performance problems that occurred during the nonroutine evolutions sampled.

April 24, 2005, Unit 1 loss of auxiliary cooling water flow

June 16, 2005, Unit 2 inadvertent energization of all pressurizer heaters

August 7, 2005, Unit 1 nuclear instrumentation power excursion to

101.87 percent nuclear instrument power

September 8, 2005, Unit 2 dropped Controlled Element Assembly 50

The inspectors completed four samples.

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Enclosure

b.

Findings

.1 Inadvertent Energization of All Unit 2 Pressurizer Heaters

Introduction. The inspectors reviewed a Green self-revealing finding involving the

unplanned energization of all Unit 2 pressurizer heaters caused by an inadequately

researched maintenance procedure.

Description. On June 1, 2005, the licensee was troubleshooting spiking in the Unit 2

pressurizer level indication using a preplanned work procedure. While in the process of

replacing Alarm Relay Bistable 2LC-4627-1BN in the indication circuitry, instrumentation

and control (I&C) technicians lifted electrical Lead 7 per the work procedure. Lifting this

lead caused a daisy chain of power losses which caused power to be lost to

Relay 63X/LC-110H in the pressurizer heater circuitry. This action in turn energized all

of the backup heaters and shunted the output of the pressurizer heater hand controller

station, thereby, fully energizing all proportional heaters. Lifting of Lead 7 also caused

the Channel 1 high pressurizer level alarm annunciator to alarm unexpectedly. With all

pressurizer heaters energized, reactor coolant system pressure rose to approximately

15 psig above normal operating pressure. In the diagnosis of the high pressurizer level

annunciator, operators recognized that all pressurizer heaters were energized, took

manual control, and restored pressure to normal. Additionally, I&C technicians

re-landed Lead 7. During inspection of this occurrence, the inspectors discovered that

the scope of the work package was inadequate, because lifting the lead had not been

properly researched by system engineers or work planners causing the unexpected

plant response.

Analysis. The inspectors determined that the licensees failure to adequately research

the effects of their maintenance on the pressurizer level circuitry was a performance

deficiency. This finding is greater than minor because it affected the human

performance attribute under the initiating events cornerstone objective of limiting the

likelihood of those events that upset plant stability and challenge critical safety functions.

Using the Phase 1 worksheets in MC 0609, "Significance Determination Process," the

issue was determined to have very low safety significance (Green) because the finding

did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation

equipment would not be available. This finding had crosscutting aspects of human

performance, in that, the engineers and planners did not adequately research a

procedure prior to its use on the plant.

Enforcement. No violation of regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because it occurred on

nonsafety-related plant equipment. Licensee personnel entered this issue into the CAP

as CR ANO-2-2005-1678. This issue is being treated as a finding:

FIN 05000368/2005004-05, "Failure to Adequately Scope the Effects of Maintenance on

Pressurizer Level Instrumentation."

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Enclosure

.2 Dropped Unit 2 CEA

Introduction. The inspectors reviewed a self-revealing Green finding for an inadequate

maintenance procedure and troubleshooting plan which resulted in a dropped CEA on

Unit 2.

Description. On September 8, 2005, during troubleshooting efforts for CEA 56, CEA 50

dropped to the bottom of the core. At the time of the event, Subgroup 13, which contain

CEAs 50 and 56, was being transferred to the hold bus to allow for replacement of the

opto-isolator card for CEA 56. Control Element Assembly 56 troubleshooting indicated

that a phase on the upper gripper was firing all the time. The troubleshooting plan that

was being used allowed for I&C maintenance personnel to transfer the rods to the hold

bus by skill of the craft. However, if operations personnel were to perform the same

task, they had specific guidance contained in Operating Procedure 2105.009, "CEDM

Control System Operation," Revision 21. As a result of not having detailed guidance in

the troubleshooting plan, not using the operations procedure as a reference and not

having familiarity from performing transfers to the hold bus on frequent bases,

I&C maintenance personnel failed to ensure that CEA 50 was latched by the upper

gripper. When I&C transferred Subgroup 13 to the hold bus, the automatic CEA timer

module detected a voltage imbalance on CEA 50 and transferred CEA 50 to the lower

gripper. Subsequently, when the contact for the normal supply to CEA 50 was opened,

power to the lower gripper was removed resulting in CEA 50 dropping to the bottom of

the core.

Analysis. The inspectors considered that the failure to provide adequate procedural

guidance for CEA transfers to I&C technicians was a performance deficiency. This

finding is greater than minor because it affected the procedure quality attribute under

the initiating events cornerstone objective of limiting those events that upset plant

stability. Using the Phase 1 worksheets in MC 0609, "Significance Determination

Process," the finding was determined to have very low safety significance (Green)

because this transient initiator does not contribute to both the likelihood of a reactor trip

and the likelihood that mitigation equipment or functions will not be available. This issue

had human performance crosscutting aspects associated with an inadequate

maintenance procedure.

Enforcement. No violation of regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because it occurred on

nonsafety-related equipment. The licensee included this condition in the CAP as

CR ANO-2-2005-2191. This issue is being treated as a finding:

FIN 05000368/2005004-06, "Inadequate Maintenance Procedure Results in Dropped

CEA."

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Enclosure

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope

For the four operability evaluations listed below, the inspectors: (1) reviewed plants

status documents such as operator shift logs, emergent work documentation, deferred

modifications, and standing orders to determine if an operability evaluation was

warranted for degraded components; (2) referred to the Updated Safety Analysis Report

and design basis documents to review the technical adequacy of licensee operability

evaluations; (3) evaluated compensatory measures associated with operability

evaluations; (4) determined degraded component impact on any Technical

Specifications; (5) used the significance determination process to evaluate the risk

significance of degraded or inoperable equipment; and (6) verified that the licensee has

identified and implemented appropriate corrective actions associated with degraded

components.

CR-ANO-1-2005-0954, July 1, 2005, Unit 1 EFW water spray system

CR-ANO-1-2005-1022, July 15, 2005, Unit 1 HELB Door 62, electrical equipment

room

CR-ANO-C-2005-1472, August 2, 2005, Units 1 and 2 molded case circuit

breakers in safety-related 480 volt switchgear

CR-ANO-C-2005-1538, August 11, 2005, Units 1 and 2 emergency cooling pond

fish eradication impact on service water systems

The inspectors completed four samples.

b.

Findings

No findings of significance were identified.

1R16

Operator Workarounds (71111.16)

a.

Inspection Scope

The inspectors reviewed the two operator workarounds listed below to: (1) determine if

the functional capability of the system or human reliability in responding to an initiating

event is affected, (2) evaluate the effect of the operator workaround on the operators

ability to implement abnormal or emergency operating procedures, and (3) verify that

the licensee has identified and implemented appropriate corrective actions associated

with operator workarounds.

August 9, 2005, Units 1 and 2 ground on Unit 1 Red Train 125V dc bus isolated

to fuses which resulted in the loss of both units control room indications for

switchyard breakers

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Enclosure

August 19, 2005, Unit 2 Operator Work Around 2-05-07 safety injection

Tank 2T-2C losing inventory excessively

The inspectors completed two samples.

b.

Findings

No findings of significance were identified.

1R17

Permanent Plant Modifications (71111.17)

Annual Review

The inspectors reviewed key affected parameters associated with energy needs,

materials/replacement components, timing, heat removal, control signals, equipment

protection from hazards, operations, flowpaths, pressure boundary, ventilation

boundary, structural, process medium properties, licensing basis, and failure modes for

the modification listed below. The inspectors verified that: (1) modification preparation,

staging, and implementation does not impair emergency/abnormal operating procedure

actions, key safety functions, or operator response to loss of key safety functions;

(2) postmodification testing will maintain the plant in a safe configuration during testing

by verifying that unintended system interactions will not occur, SSC performance

characteristics still meet the design basis, the appropriateness of modification design

assumptions, and the modification test acceptance criteria has been met; and (3) the

licensee has identified and implemented appropriate corrective actions associated with

permanent plant modifications.

August 12, 2005, Unit 1 reactor vessel closure head replacement per

ER-ANO-2002-0638-000

The inspectors completed one sample.

b.

Findings

No findings of significance were identified.

1R19

Postmaintenance Testing (71111.19)

a.

Inspection Scope

The inspectors selected the six postmaintenance test activities of risk significant

systems or components listed below. For each item, the inspectors: (1) reviewed the

applicable licensing basis and/or design-basis documents to determine the safety

functions; (2) evaluated the safety functions that may have been affected by the

maintenance activity; and (3) reviewed the test procedure to ensure it adequately tested

the safety function that may have been affected. The inspectors either witnessed or

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Enclosure

reviewed test data to verify that acceptance criteria were met, plant impacts were

evaluated, test equipment was calibrated, procedures were followed, jumpers were

properly controlled, the test data results were complete and accurate, the test

equipment was removed, the system was properly realigned, and deficiencies during

testing were documented. The inspectors also reviewed the CAP to determine if the

licensee identified and corrected problems related to postmaintenance testing.

March 21, 2005, Unit 2 HPSI Pump 2P-89C, troubleshooting to determine source

of increased vibration levels

June 21, 2005, Unit 1 HPI Pump P-36B inboard motor bearing oiler unqualified

for application

August 16, 2005, Unit 2 excore Channel B power supply switch replacement

August 18, 2005, Units 1 and 2 control room ventilation Valve SV-7910, outside

air makeup damper for control room ventilation Fan VSF-9, replacement

August 19, 2005, Unit 1 instrument air Compressor C-28A air end replacement

August 31, 2005, Unit 2 service water Valve 2CV-1519 stroke failure

The inspectors completed six samples.

b.

Findings

No findings of significance were identified.

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope

For the five surveillances listed below, the inspectors reviewed the Updated Safety

Analysis Report, procedure requirements, and Technical Specifications to ensure they

demonstrated that the SSCs tested were capable of performing their intended safety

functions. The inspectors either witnessed or reviewed test data to verify that the

following significant surveillance test attributes were adequate: (1) preconditioning;

(2) evaluation of testing impact on the plant; (3) acceptance criteria; (4) test equipment;

(5) procedures; (6) jumper/lifted lead controls; (7) test data; (8) testing frequency and

method demonstrated Technical Specification operability; (9) test equipment removal;

(10) restoration of plant systems; (11) fulfillment of ASME Code requirements;

(12) updating of performance indicator data; (13) engineering evaluations, root causes,

and bases for returning tested SSCs not meeting the test acceptance criteria were

correct; (14) reference setting data; and (15) annunciators and alarms setpoints. The

inspectors also verified that the licensee identified and implemented any needed

corrective actions associated with the surveillance testing.

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Enclosure

January 1 through July 31, 2005, Unit 2 emergency cooling pond level detection

July 13, 2005, Unit 2 HPSI header check Valve 2SI-12

July 14, 2005, Unit 1 control room emergency ventilation system inlet

Damper CV-7910

August 2, 2005, Unit 2 containment air monitoring system

Instrument 2RITS-8231-1A (Leakage Detection System)

August 25, 2005, Unit 1 low pressure injection Pump P-34B (Inservice Test)

The inspectors completed five samples.

b.

Findings

No findings of significance were identified.

1R23

Temporary Plant Modifications (71111.23)

a.

Inspection Scope

For the three temporary modifications listed below, the inspectors reviewed the Updated

Safety Analysis Report, plant drawings, procedure requirements, and Technical

Specifications to ensure that the temporary modifications were properly implemented.

The inspectors: (1) verified that the modification did not have an affect on system

operability/availability, (2) verified that the installation was consistent with the

modification documents, (3) ensured that the postinstallation test results were

satisfactory and that the impact of the temporary modification on permanently installed

SSCs were supported by the test, (4) verified that the modifications were identified on

control room drawings and that appropriate identification tags were placed on the

affected drawings, and (5) verified that appropriate safety evaluations were completed.

The inspectors verified that the licensee identified and implemented any needed

corrective actions associated with temporary modifications.

July 21, 2005, Unit 1 control room emergency ventilation system inlet

Damper CV-7910

July 28, 2005, Unit 2 pressurizer level instrumentation

August 30 through September 1, 2005, Unit 1 makeup Pump P-36A temporary

wall removal

The inspectors completed three samples.

-18-

Enclosure

b.

Findings

No findings of significance was identified.

Cornerstone: Emergency Preparedness

1EP2 Alert Notification System Testing (71114.02)

a.

Inspection Scope

The inspector discussed with the licensee and staff from the Arkansas Department of

Health the status of offsite siren and tone alert radio systems to determine the adequacy

of methods for testing the alert and notification system in accordance with

10 CFR Part 50, Appendix E. The Arkansas Department of Healths alert and

notification system testing program was compared with criteria in NUREG-0654,

"Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants," Revision 1, Federal Emergency

Management Agency (FEMA) Report REP-10, "Guide for the Evaluation of Alert and

Notification Systems for Nuclear Power Plants," and the current FEMA-approved alert

and notification system design report. The inspector also reviewed the following

procedures:

"Procedures for Testing, Verification, and Maintenance of the Emergency

Warning System," Arkansas Department of Health, May 2004, Revision 0

Desk Guide EP-002, "Early Warning System," Revision 10

b.

Findings

No findings of significance were identified.

1EP3 Emergency Response Organization Augmentation Testing (71114.03)

a.

Inspection Scope

The inspector reviewed results from two emergency response staffing drills and

reviewed the following documents related to the emergency response organization

augmentation system to determine the licensees ability to staff emergency response

facilities in accordance with the licensee emergency plan and the requirements of

10 CFR Part 50, Appendix E.

Procedure 1903.062, "Communication System Operating Procedure,"

Revision 18

Form 1903.062C, "Emergency Response Staffing Drill," Revision 18

-19-

Enclosure

b.

Findings

No findings of significance were identified.

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

a.

Inspection Scope

The inspector reviewed the following documents related to the licensees CAP to

determine the licensees ability to identify and correct problems in accordance with

10 CFR 50.47(b)(14) and 10 CFR Part 50, Appendix E.

EN-LI-102, "Corrective Action Process," Revision 1

Emergency Preparedness CR Threshold Criteria, Revision 0

Seven quarterly department assessments

Three Entergy peer group assessments

LO-ALO-2003-234, "Alert Notification System Assessment," December 8, 2003

LO-ALO-2005-033, "Emergency Preparedness Department Program

Assessment," April 2005

Five evaluation reports for full scale drills

Two evaluation reports for emergency preparedness drills

NQ 2004-0026, "Quality Assurance Audit Report QA-7-2004-ANO-1, Emergency

Planning," June 8, 2004

02C-ANO-2003-0055, Quality Assurance Observation

Summaries of 176 corrective actions assigned to the emergency preparedness

department between July 1, 2003, and June 1, 2005

b.

Findings

No findings of significance were identified.

1EP6 Drill Evaluation (71114.06)

a.

Inspection Scope

The two drills listed below contributed to drill/exercise performance and emergency

response organization (ERO) performance indicators. The inspectors: (1) observed the

-20-

Enclosure

training evolution to identify any weaknesses and deficiencies in classification,

notification, and protective action requirements development activities; (2) compared the

identified weaknesses and deficiencies against licensee identified findings to determine

whether the licensee is properly identifying failures; and (3) determined whether licensee

performance is in accordance with the guidance of NEI 99-02, "Regulatory Assessment

Indicator Guideline," Revision 2, documents acceptance criteria.

July 20, 2005, emergency response organization drill involving a station blackout

initiated from the Unit 2 simulator and activating the Technical Support Center,

Emergency Operations Facility, and Operations Support Center

July 27, 2005, emergency response organization drill involving a station blackout

initiated from the Unit 2 simulator and activating the Technical Support Center,

Emergency Operations Facility, and Operations Support Center

The inspectors completed two samples.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

a.

Inspection Scope

The inspector sampled the licensee's performance indicator submittals listed below for

the period October 1, 2004, through March 31, 2005. The definitions and guidance of

NEI 99-02, "Regulatory Assessment Indicator Guideline," Revision 2, were used to verify

the licensees basis for reporting each data element in order to verify the accuracy of

performance indicator data reported during the assessment period. Licensee

performance indicator data were also reviewed against the requirements of

Procedures EN-LI-114, "Performance Indicator Process," Revision 0; EN-EP-201,

"Emergency Planning Performance Indicators," Revision 1; and EPJA-EOF-21,

"Emergency Preparedness Performance Indicators," Revision 0.

Emergency Preparedness Cornerstone:

Drill and exercise performance

Emergency response organization participation

Alert and notification system reliability

The inspector reviewed a 100 percent sample of drill and exercise scenarios, licensed

operator simulator training sessions, notification forms, and attendance and critique

records associated with training sessions, drills, and exercises conducted during the

verification period. The inspector reviewed licensee emergency response rosters and

-21-

Enclosure

drill participation records. The inspector reviewed alert and notification system testing

procedures, maintenance records, and a 100 percent sample of siren test records. The

inspector also interviewed licensee personnel responsible for collecting and evaluating

performance indicator data.

b.

Findings

No findings of significance were identified.

4OA2 Problem Identification and Resolution

.1

Emergency Preparedness Annual Sample Review

a.

Inspection Scope

The inspector selected 30 CRs for detailed review. The reports were reviewed to

ensure that the full extent of the issues were identified, an appropriate evaluation was

performed, and appropriate corrective actions were specified and prioritized. The

inspector evaluated the CRs against the requirements of Procedure EN-LI-102,

"Corrective Action Process," Revision 1.

b.

Findings

No findings of significance were identified.

.2

Daily Reviews

a.

Inspection Scope

The inspectors performed a daily review of all condition reports entered into the licensee

corrective action program during this inspection period to identify repetitive failures and

human performance issues. These daily reviews also assessed licensee identification

of issues at the appropriate threshold and entry of these issues into their corrective

action program.

4OA3 Event Followup (71153)

(Closed) Licensee Event Report (LER) 05000368/2002001-00, Reactor Coolant System

Pressure Boundary Leakage Due To Primary Water Stress Corrosion Cracking of

Pressurizer Heater Sleeves

During the Unit 2 refueling outage in April and May 2002, the licensee discovered that

the reactor coolant system had leaked through six pressurizer heater sleeves. The

inspectors previously reviewed these leaks and documented the review in NRC

Inspection Report 05000313/2004002; 05000368/2004002, but this LER was not closed

pending the characterization of the metallurgical flaws which caused these leaks. The

inspectors discovered that the licensee does not intend to characterize the flaws on the

-22-

Enclosure

Unit 2 pressurizer because the existing flaws have been repaired and because they

have planned to replace the pressurizer in Fall 2006. Additionally, the inspectors

reviewed a similar event in NRC Inspection Report 0500313/2005003;

0500368/2005003 (Section 4OA3.2) in which LER 0500368/2005001-00 was closed for

the same issue, leaking pressurizer heater sleeves. For further information of this

previously dispositioned violation, see NRC Inspection Report 0500313/2004002;

00500368/2004002 (Section 4OA3.2) NCV 050036/2004-002, "Ineffective Corrective

Actions to Prevent Recurrence of Primary Water Stress-Corrosion Cracking of Alloy 600

Material." As a result, the inspectors foresee no needed future inspection of this LER.

This LER is closed.

4OA4 Crosscutting Aspects of Findings

Cross-Reference to Human Performance Findings Documented Elsewhere

Section 1R13 describes a condition where maintenance personnel failed to

communicate to Unit 1 operations the status of Door 5, which resulted in operations not

being able to ensure that the required controls were exercised. This same finding also

documents an inadequate work package in that the correct ERs were not listed, which

resulted in risk management actions not being implemented.

Section 1R13 describes a finding where operations personnel incorrectly assumed

isolation of the Unit 1 ERV would have no impact on plant risk, which resulted in an

inadequate risk assessment.

Section 1R14 describes a condition where engineers and work planners did not

adequately research a troubleshooting procedure which resulted in energization of all

Unit 2 pressurizer heaters.

Section 1R14 describes a condition where an inadequate maintenance procedure

resulted in a Unit 2 CEA falling into the core. The procedure lacked the necessary

guidance because the task of transferring control element assemblies to the hold bus

was viewed as skill of the craft even though such evolutions are infrequently

performed.

4OA5 Other Activities

.1

Followup to Operational Readiness of Offsite Power (Temporary

Instruction (TI) 2515/163)

The inspectors conducted followup inspection to TI 2515/163, "Operational Readiness of

Offsite Power," to determine the extent of the licensees written guidance on various

aspects of the TI. The results were forwarded to the Division of Engineering in the

Office of Nuclear Reactor Regulation for further review.

-23-

Enclosure

.2

(Closed) Apparent Violation 05000368/2005003-01, Inadequate Procedure Leads To

Reactor Coolant Pump Seal Damage

Introduction. The inspectors completed the significance determination of the apparent

violation documented in NRC Inspection Report 05000313/2005003 and

05000368/2005003. The apparent violation involved an inadequate procedure related to

the alignment of reactor coolant pump (RCP) seal injection flow when the pump and

motor were uncoupled. An additional entry into reduced reactor coolant system (RCS)

inventory conditions during the refueling outage was necessary to repair the damaged

RCP seal caused by this performance deficiency.

Analysis. The inspectors considered that the failure to have an adequate procedure for

ensuring isolation of seal injection when a Unit 2 reactor coolant pump was uncoupled

was a performance deficiency. Traditional enforcement does not apply for this finding

because it did not have any actual safety consequences or potential for impacting the

NRCs ability to perform its regulatory function nor was it the result of any willful violation

of NRC requirements. The inspectors determined that this finding is greater than minor

because it was associated with the Mitigating Systems Cornerstone configuration control

attribute and affected the cornerstones objective of ensuring the availability, reliability,

and capability of systems that respond to initiating events to prevent undesirable

consequences.

The inspectors used Appendix G, "Shutdown Operations Significance Determination

Process," of MC 0609, "Significance Determination Process," to further determine the

significance of this finding.

Unplanned entry into reduced RCS inventory conditions to repair the RCP seal

represented additional risk incurred above the planned outage risk. The additional risk

associated with the reduced RCS inventory evolution constitutes the additional risk

incurred above the planned outage risk. A Phase 1 screening of the finding was

performed using Appendix G and the Attachment 1 checklists. The finding was not

considered a "Loss of Control" using Table 1. Using Checklist 3, "PWR Cold Shutdown

and Refueling Operation - RCS Open and Refueling Cavity Level < 23' Or RCS Closed

and No Inventory in Pressurizer, Time to Boiling < 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />," in Attachment 1, "Phase 1

Operational Checklists for both PWRs and BWRs," of Appendix G of MC 0609, the

inspectors determined this finding required quantitative assessment because the finding

increased the likelihood of a loss of RCS inventory by requiring an additional entry into a

reduced RCS inventory condition. Therefore, the finding was referred to the regional

senior reactor analyst for further evaluation.

Since the finding did not involve low temperature overpressure protection, nozzle dams,

or boron dilution, the analyst used Appendix G, Attachment 2, "Phase 2 SDP Template

for PWR During Shutdown." The finding involved an additional entry into a high-risk

Plant Operating State (POS). Therefore, as cautioned in Attachment 2, the senior

reactor analyst consulted with staff in the Office of Nuclear Reactor Regulation to

evaluate the change in core damage frequency associated with the finding. The

following is a summary of the analysis that was performed.

-24-

Enclosure

After review of Appendix G and its associated technical basis document MC 0308,

Attachment 3, Appendix G, the analysts concluded that the applicable initiators for this

condition were the loss of offsite power (LOOP), loss of residual heat removal (LORHR),

and loss of inventory (LOI). The analysts considered loss of level control (LOLC) as a

potential initiator, but rejected it because the LOLC worksheet was only applicable to

midloop RCS conditions and the performance deficiency resulted in an additional drain

only to RCP seal replacement elevation. The analysts concluded that solution of each

of the applicable initiator worksheets at their "base case" value was an appropriate

conservative estimation of the increase in risk due to the finding.

The additional entry into reduced inventory conditions occurred approximately 28 days

after shutdown for the refueling outage and lasted approximately 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> (< 3 days).

These conditions correlate to the Late Time Window (TW-L) of POS 2 in the SDP and

were used to solve each of the following initiators:

LOOP

Worksheet 4, "Loss of Offsite Power in POS 2 (RCS Vented)," was evaluated. The

initiating event likelihood (IEL) for the LOOP initiator for exposure less than 3 days is 3.

The analyst reviewed the top event functions, equipment success criteria, and important

instrumentation identified in Worksheet 4 to determine appropriate equipment credits to

evaluate the core damage sequences. Top event function EAC was assigned a credit of

4, accounting for the emergency and alternate a.c. diesel generators. The analysts

assumed that operator credit was similar to equipment credit for this top event and

made no reduction for operator error. Gravity feed to the RCS was not credited.

Recovery of offsite power was assigned a credit of 1. Quantification of the sequences

by summing the IEL and mitigation credits for each top event function resulted in the

most limiting sequence having a result of 8.

LORHR

Worksheet 9, "Loss of RHR in POS 2 (RCS Vented)," was evaluated. The IEL for the

LORHR initiator for exposure less than 3 days is 3. The analyst reviewed the top event

functions, equipment success criteria, and important instrumentation identified in

Worksheet 9 to determine appropriate equipment credits to evaluate the core damage

sequences. Top event function RHR-S was assigned a credit of 1, which credited

operator ability to start a decay heat removal train prior to RCS boiling. Top event FEED

was assigned a credit of 4 accounting for the multi-train safety injection system and

positive displacement charging pumps. Operator credit was also 4 for this top event, so

no reduction was applied. Top event RHR-R was assigned a credit of 2, consistent with

the worksheet for being operator-action limited. Top event RWSTMU was also assigned

a credit of 2, consistent with the worksheet for being operator-action limited.

Quantification of the sequences by summing the IEL and mitigation credits for each top

event function resulted in the most limiting sequence having a result of 8.

-25-

Enclosure

LOI

Worksheet 6, "Loss of Inventory in POS 2 (RCS Vented)," was evaluated. The IEL for

the LOI initiator for exposure less than 3 days is 4. The analyst reviewed the top event

functions, equipment success criteria, and important instrumentation identified in

Worksheet 6 to determine appropriate equipment credits to evaluate the core damage

sequences. Top event function FEED was assigned a credit of 4 accounting for the

multi-train safety injection system and positive displacement charging pumps. Operator

credit was also 4 for this top event, so no reduction was applied. Top event LEAK-

STOP was assigned a credit of 3, limited by operator action. Top event RHR-R was

assigned a credit of 3, consistent with the worksheet for being operator-action limited.

Top event RWSTMU was assigned a credit of 2, consistent with the worksheet for being

operator-action limited. Quantification of the sequences by summing the IEL and

mitigation credits for each top event function resulted in the most limiting sequence

having a result of 8.

Result

The risk significance of the finding from this point is determined in the same manner as

for at-power findings. Using MC 0609, Appendix A, Step 2.4, "Estimating the Risk

Significance of Inspection Findings," the analyst summed the quantified sequences and

determined that the total increase in core damage frequency associated with this finding

due to internal initiating events was estimated as 1E-7/year using the counting rule. No

screening for potential contribution due to external events or large early release

frequency was performed because of the assumed conservative upper-bound screening

result provided by the SDP worksheets. Therefore, this was a finding of very low safety

significance (Green). Contributing to this result was that (1) the seal replacement

activity required RCS draindown to reduced inventory conditions and not to midloop

conditions, (2) the time needed to replace the seal was not extensive and, (3) the time

after shutdown provided additional time available for successful operator actions.

Enforcement. The inspectors determined that since Procedure 2103.002, "Filling and

Venting the Reactor Coolant System," Revision 39, was inadequate, it did not meet the

requirements of Regulatory Guide 1.33, Revision 2, Appendix A, February 1978, and as

a result the licensee did not meet Unit 2 Technical Specification 6.4.1, "Procedures."

Because of the very low safety significance of this finding and because the licensee

included this condition in their CAP as CR ANO-2-2005-0545, this violation is being

treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000368/2005004-07, "Inadequate Procedure Leads To Reactor Coolant Pump

Seal Damage."

-26-

Enclosure

4OA6 Meetings, Including Exit

On July 1, 2005, the inspector presented the emergency planning inspection results to

Mr. J. Forbes, Vice President, Operations, and other members of the licensee's staff

who acknowledged the findings. The inspector confirmed that proprietary information

was not provided or examined during the inspection.

The inspectors debriefed the licensee's operator requalification inspection results with

Ms. S. Cotton, Training Manager, and other members of the licensees staff at the

conclusion of the inspection on July 15, 2005. The licensee acknowledged the findings

presented. A telephone exit was held with Mr. R. Martin, Unit 1 Operations Training

Supervisor, acting for Ms. S. Cotton, on August 17, 2005. He was advised that the

inspectors had completed reviewing the results of the annual requalification test results

for Unit 2 and the biennial requalification test results for Unit 1. The inspectors asked

the licensee whether any materials examined during the inspection should be

considered proprietary. No proprietary information was identified.

The inspectors presented the inspection results to Mr. J. Forbes, Vice President,

Operations, and other members of the licensee's staff at the conclusion of the heat sink

performance biennial inspection on September 12, 2005, during a telephonic exit. No

proprietary information was reviewed.

The resident inspectors presented the inspection results of the resident inspections to

Mr. J. Forbes, Vice President, Operations, and other members of the licensee's

management staff on September 28, 2005. The licensee acknowledged the findings

presented. The inspectors noted that while proprietary information was reviewed, none

would be included in this report.

4OA7 Licensee-Identified Violations

The following two examples of a violation of very low safety significance (Green) were

identified by the licensee and are violations of NRC requirements which meet the criteria

of Section VI of NUREG-1600, "NRC Enforcement Policy," for being dispositioned as

NCV.

10 CFR Part 50, Appendix B, Criterion III, "Design Control," requires, in part, that

measures shall be established for the selection and review of materials, parts,

equipment, and processes that are essential to safety-related functions. The licensee

violated this requirement on two occasions. The first example, which occurred on

March 21, 2005, during the Unit 2 HPSI Pump 2P-89C disassembly troubleshooting, to

determine the source of increased vibration levels, the licensee discovered that a carbon

steel set screw had been installed in place of a stainless one required by design

specifications. This event is documented in the licensees CAP as

CR ANO-2-2005-0775. This finding is of very low safety significance because the

safety-related function of the HPSI system was never lost. The second example, which

occurred on June 21, 2005, during the Unit 1 HPI Pump P-36B gearbox rebuild, the

licensee installed an unqualified bearing oiler on the inboard motor bearing which

-27-

Enclosure

caused increased vibrations of the oiler. This event is documented in the licensees

CAP as CR ANO-1-2005-0884. This finding is of very low safety significance because

the safety-related function of the HPI system was never lost.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment 1

A-1

KEY POINTS OF CONTACT

Licensee Personnel

R. Barnes, Manager, Planning and Scheduling

S. Bennett, Project Manager, Licensing

B. Berryman, Manager, Unit 1 Operations

E. Blackard, Supervisor, Mechanical Design Engineering

J. Browning, Manager, Unit 2 Operations

R. Byford, Training Supervisor/Operations Training

A. Clinkingbeard, U-1 Operations Training Assistant Operations Manager

S. Cotton, Manager, Training

S. Cupp, Simulator Support Supervisor

J. Eichenberger, Manager, Corrective Actions and Assessments

J. Forbes, Vice President, Operations

N. Finney, Technical Specialist IV, Non-Destructive Examination

M. Ginsberg, Supervisor, Design Engineering

A. Hawkins, Licensing Specialist

J. Hoffpauir, Manager, Maintenance

R. Holeyfield, Manager, Emergency Planning

I. Jacobson, System Engineer

D. James, Acting Director, Nuclear Safety Assurance

W. James, Manager, Alloy 600 Group

J. Johnson, Fire Protection Technical Specialist

J. Kowalewski, Director, Engineering

R. Kowalewski, Manager, Technical Support

D. Lomax, Manager, Dry Fuels

R. Martin, U-1 Operations Training Supervisor

T. Mayfield, U-2 Operations Training Supervisor

J. Miller, Manager, Systems Engineering

T. Mitchell, Acting General Manager, Plant Operations

D. Moore, Manager, Radiation Protection

K. Nichols, Manager, Design Engineering

R. Puckett, Fire Protection Supervisor

S. Pyle, Licensing Specialist

C. Reasoner, Manager, Engineering Programs and Components

R. Scheide, Licensing Specialist

J. Sigle, U-2 Acting Operations Manager

C. Tyrone, Manager, Quality Assurance

F. Van Buskirk, Licensing Specialist/ANO Licensing

B. Williams, Director, Reactor Vessel Head/SG Replacement Project

Arkansas Department of Health

C. Meyer, Nuclear Planning and Response Program Manager

Attachment 1

A-2

NRC

R. Kahler, NSIR/DPR/EPD, Team Leader

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000313/2005004-01

URI

Failure to Comply with Licensing Basis for EFW Pump

Room Fire Sprinklers (Section 1R05)05000313/2005004-02

URI

Absence of ICS Relay Room Fire Sprinklers

(Section 1R05)

Opened and Closed

05000313/2005004-03

NCV

Failure to Adequately Assess Risk for a Blocked Decay

Heat Vault Door (Section 1R13)05000313/2005004-04

NCV

Failure to Adequately Assess Risk for an Isolated

Pressurizer ERV (Section 1R13)05000368/2005004-05

FIN

Failure to Adequately Scope the Effects of Maintenance

on Pressurizer Level Instrumentation (Section 1R14)05000368/2005004-06

FIN

Inadequate Maintenance Procedure Results in Dropped

CEA (Section 1R14)05000368/2005004-07

NCV

Inadequate Procedure Leads to Reactor Coolant Pump

Seal Damage (Section 4OA5)

Closed

05000368/2002-001-00

LER

Reactor Coolant System Pressure Boundary Leakage

Due to Primary Water Stress Corrosion Cracking of

Pressurizer Heater Sleeves (Section 4OA3)05000368/2005003-01

AV

Inadequate Procedure Leads to Reactor Coolant Pump

Seal Damage (Section 4OA5)

Discussed

None

Attachment 1

A-3

LIST OF DOCUMENTS REVIEWED

In addition to the documents referred to in the inspection report, the following documents were

selected and reviewed by the inspectors to accomplish the objectives and scope of the

inspection and to support any findings:

Section 1R04: Equipment Alignment

CRs

ANO-2-2004-0620

ANO-2-2004-0702

ANO-2-2004-0837

ANO-2-2004-0922

ANO-2-2004-0936

ANO-2-2004-1704

ANO-2-2004-2054

ANO-2-2004-2055

ANO-2-2004-2091

ANO-2-2005-0387

ANO-2-2005-1193

ANO-2-2005-1424

ANO-2-2005-1921

ANO-2-2005-1927

Operating Procedures

NUMBER

TITLE

REVISION

2104.005

Containment Spray

43

Miscellaneous

NUMBER

TITLE

ULD-2-SYS-05

Arkansas Nuclear One Upper Level Document ANO

Unit 2 Containment Spray System

3

Section 1R05: Fire Protection

CRs

ANO-1-2005-0954

ANO-1-2005-1197

Engineering Calculation

85-E-0053-15, Revision 45

Miscellaneous Documents

NUMBER

TITLE

REVISION

DCP 87-D-1051

EFW Pump Room Fire Suppression System

0

Engineering

Report A-FP-2005-001

Fire Protection Appendix R Detection & Suppression

Partial 86-10 Evaluation

0

NFPA 15

Standard for Water Spray Fixed Systems for Fire

Protection

1985

Edition

Attachment 1

A-4

NFPA 15

Standard for Water Spray Fixed Systems for Fire

Protection

2001

Edition

NRC Information Notice 2002-24

Potential Problems with Heat Collectors on Fire

Protection, Sprinklers

July 19,

2002

0CAN088404

Results of Reanalysis Against NRC

Clarification/Interpretation of Appendix R to

10 CFR Part 50

August 15,

1984

0CAN088508

Results of Reanalysis Against NRC

Clarification/Interpretation of Appendix R to

10 CFR Part 50 - Supplemental Information

August 30,

1985

1CAN048708

10 CFR Part 50 Appendix R Exemption Request

(Zone 38-Y)

April 22,

1987

1CAN068706

10 CFR Part 50 Appendix R Exemption Request

(Zone 38-Y)

June 24,

1987

1CNA108806

Exemptions from the Technical Requirements of

Appendix R to 10 CFR Part 50 - Arkansas Nuclear

One, Unit 1 (TAC NO. 55669)

October 26,

1988

Operating Procedures

NUMBER

TITLE

REVISION

Arkansas Nuclear One Fire Hazards Analysis Report

9

Unit 1 Prefire Plans 1A-372-100-N

2

1000.152

Unit 1 & 2 Fire Protection System Specifications

3

1203.002

Alternate Shutdown

15

1203.049

Fires in Areas Affecting Safe Shutdown

2

Plant Drawings

NUMBER

TITLE

REVISION

FP-103

Fire Zones Intermediate Floor Plan at Elev. 368' - 0"

and 372' - 0"

24, Sheet 1

FP-105

Fire Zone Plan Below Grade Elev. 335' - 0"

18, Sheet 1

FP-110

Fire Zones Intake Structure

10, Sheet 1

FP-2103

Fire Zones Intermediate Floor Plan Elev. 368' - 0"

26, Sheet 1

Attachment 1

A-5

Section 1R06: Flooding

Engineering Report

92-R-0024-01

Section 1R07: Heat Sink Performance

Operating Procedures

NUMBER

TITLE

REVISION

2311.002

Service Water System Flow Test

14

EN-LI-102

Corrective Action Process

2

Unit 1 and Unit 2 Service Water and Circulating Water

Optimization Plan

1

Specifications

ANO FSAR Unit 2, Section 6.3.4, "Tests and Inspections"

ERs

NUMBER

TITLE

REVISION

ANO-2004-0294-000

Decay Heat Cooler Thermal Test Evaluation

0

ANO-2005-0287-000

2R17 As Left Test Evaluation

0

991457-E205-0

Service Water Flow Testing

0

ANO-2004-0294-000

1R18 E-35A Decay Heat Cooler Thermal Test

Evaluation

0

CRs

ANO-1-2004-0831

ANO-2-1999-0211

ANO-2-1999-0219

ANO-2-1999-0254

ANO-2-1999-0580

ANO-2-1999-0535

ANO-2-1999-0559

Calculations

NUMBER

TITLE

REVISION

88-E-0098-16

Revised Containment Cooler Data for ANO

001

94-E-0095-18

Room 2007/2009 Heat Load Evaluation

0

88-E-0098-20

Heat Load Evaluation

0

88-E-0098-20

ANO-1 DBA Analysis

1

Attachment 1

A-6

98-E-0022-05

Decay Heat Removal Cooler E-35B 1R16 Thermal

Performance Test

001

94-E-0095-2014

Heat load Evaluation

1

98-E-0022-03

Decay Heat Removal Cooler E-35A 1R15 Thermal

Performance Test

0

98E-0022-04

Decay Heat Removal Cooler E-35B 1R215 Thermal

Performance Test

0

Testing Procedures and Results

NUMBER

TITLE

REVISION

98-E-0022-02

Decay Heat Removal Cooler E-35A, Thermal

Performance Test

0

98-E-0022-04

Decay Heat Removal Cooler E35B, 1R15, Thermal

Performance Test

0

98-E-0022-03

Decay Heat Removal Cooler E-35A,1R15, Thermal

Performance Test

0

98E-0022-03

Decay Heat Removal Cooler E-35B, 1R16, Thermal

Performance Test

0

Section 1R11: Licensed Operator Requalification

OLTS Report 9 list (NRC)

ANO Unit 1 licensed operator training list

Open Simulator Discrepancy Report (reviewed all 44 records)

Closed Simulator discrepancy report from January 2003 through July 11, 2005 (reviewed

600 records) with the following detailed package reviews:

DR 05-0079, closed, topic was emergency diesel generator loading rates

DR 05-0081, closed, topic was main turbine response to loss of all steam

DR 02-0244, closed, topic was heater drain pump impact on main feed system flows

and pressures

DR 03-0073, closed, topic was heater drain tank level and recirc valve position

DR 03-0090, closed, topic was heater drain tank level control after drain pump trip

DR 03-0117, closed, topic was heater drain tank high level bypass capacity

Attachment 1

A-7

DR 03-0202, closed, topic was OTSG levels posttrip

DR 05-0075, closed, topic was reactor trip setpoints

LER 50-313-2003-001, August 29, 2003, "Reactor Trip due to Automatic Actuation of the

Reactor Protection System on High Reactor Coolant System Pressure and Actuation of the

EFW System Resulting from a Lightning-Induced Closure of the Main Turbine Governor Valves,"

Corresponding simulator file, Attachment R-15

Annual Operability Test packages

Steady state power test (100 percent)

Transients Reviewed:

Simultaneous closure of both main steam isolation valves

Trip of one reactor coolant pump

Maximum rate power ramp

Real time test package

SBT package - reviewed one scenario package with a loss of offsite power as the main event

Simulator Core Reload Acceptance Test, DG-TRNA-015-CORETEST, Revision 0, with

enclosed Unit 1 attachments

Simulator CAE file for Heater Drain Pump B trip test, Attachment R-14

STM 1-20, Figure 20-01, "Simplified Condensate System," Revision 7

PID 205, Sheet 2, "Condensate System"

Latest PSA Risk Table for Unit 1 Highest Risk Operator Actions, October 2004

Simulator Modification Control, DG-TRNA-015-SIMCONTROL, Revision 0

Simulator Configuration Control, EN-TQ-202, Revision 0

Scenarios: SES-1-004, SES-1-019

JPMs A1JPM-RO-EOP01, -EOP04, -PZR02, -EAL06, -AOP14, and -EDG05

Operations On-Shift Training Instruction Plan: "Mode 3 Operation Contingencies"

Operating Procedures

NUMBER

TITLE

REVISION

1063.008

Operations Training Sequence

34

EN-TQ-201

Systematic Approach to Training

0

TQF-201-1M05

Remedial Training Plan

2

ENS-NS-112

Medical Program and Physicals

3

Attachment 1

A-8

CR ANO-1-2003-00796, P-8A heater drain pump trip on July 25, 2003

Root Cause Analysis Report, "P-8A Heater Drain Pump Motor Winding Failure,"

September 10, 2003

CR ANO-1-2003-00987, P-8B heater drain pump trip on September 19, 2003

Root Cause Analysis Report, "Failure to Meet Reactivity Management Expectations," dated

December 1, 2004

Section 1R12: Maintenance Effectiveness

CRs

ANO-2-2003-1257

ANO-2-2003-1567

ANO-2-2003-1574

ANO-2-2003-1575

ANO-2-2003-1591

ANO-2-2003-1680

ANO-2-2004-0041

ANO-2-2004-0379

ANO-2-2004-0389

ANO-2-2004-0784

ANO-2-2004-1103

ANO-2-2004-1916

ANO-2-2005-0385

ANO-2-2005-0414

ANO-2-2005-0807

ANO-2-2005-0995

ANO-2-2005-2006

ANO-2-2005-2111

Miscellaneous

Maintenance Rule Database, Unit 2 HPSI

System Performance Indicator, HPSI - Arkansas Unit 2

Section 1R13: Maintenance Risk Assessments and Emergent Work Control

CR

ANO-C-2005-1205

ERs

963555 I103

963555 R101

963555 R112

ANO-1996-3555-056

Miscellaneous

MAI 74687

Procedures

NUMBER

TITLE

REVISION

1000.152

Unit 1 & 2 Fire Protection System Specifications

3

1000.120

ANO Fire Watch Program

10

COPD024

Risk Assessment Guidelines

16

Attachment 1

A-9

Work Order 50268810 01

Section 1R14: Operator Performance During Nonroutine Plant Evolutions and Events

CRs

ANO-2-2005-1969

ANO-2-2005-2193

ANO-2-2005-2191

ANO-2-2005-2192

Operating Procedures

NUMBER

TITLE

REVISION

2203.003

CEA Malfunction

15

2105.009

CEDM Control System Operation

21

Work Order 00070272 01

Section 1R16: Operator Workarounds

CR

ANO-C-2005-1520

Section 1R19: Postmaintenance Testing

CRs

ANO-1-2005-0884

ANO-1-2005-0895

ANO-1-2005-0900

ANO-1-2005-1208

ANO-2-1997-0055

ANO-2-2005-0385

ANO-2-2005-0659

ANO-2-2005-0747

ANO-2-2005-0775

ANO-2-2005-0782

ANO-2-2005-0948

ANO-2-2005-1673

ANO-2-2005-1754

ANO-2-2004-1923

ANO-C-2005-1593

ER

ANO-2002-0083-000

Work Orders

00057097 03

00063471 01

00063618 01

00064655 01

00069039 01

00071184 01

00071637 01

00071637 03

50254113 01

50967812 01

50976843 01

50976851 01

50999668 01

51006765 01

51006909 01

51007157 01

Attachment 1

A-10

Section 1R22: Surveillance Testing

CRs

ANO-C-2004-0353

ANO-C-2005-1218

ER

ANO-2003-0235, Revisions 0 and 1

Miscellaneous

NUMBER

TITLE

REVISION

TD V085.0080

Maintenance Manual for Velan 2 1/2" - 24" Forged

Bolted Bonnet Gate and Globe Valves and Bolted

Cover Check Valves

N/A

TD V085.0040

Maintenance Manual for Velan 2" - 24" Cast and

Forged Pressure Seal Gate, Globe Parallel Slide and

Check Valves

N/A

TD V085.0060

Instruction Manual for Installation, Operation and

Maintenance of Velan Pressure Seal Forged Gate,

Stop, Stop Check, and Check Valves

N/A

Operating Procedures

NUMBER

TITLE

REVISION

2104.005

Containment Spray

43

2104.007

Control Room Emergency Air Conditioning and

Ventilation

27

2104.039

HPSI System Operation

42

2304.006

Unit 2 Gaseous Process Radiation Monitoring

System Calibration

17

2304.016

Unit 2 Process Radiation Monitoring Monthly Test

16

2402.143

Disassembly, Inspection and Reassembly of 2SI-12

1

Work Orders

00067969 02

50618124 01

50967615 01

50967812 01

51003781 01

Attachment 1

A-11

1EP2: Alert and Notification System Testing

Alert and Notification System Report for Arkansas Nuclear One, Revised February 13, 1996

1EP3: Emergency Response Organization Augmentation

Emergency Response Staffing Drill, December 2004

Emergency Response Staffing Drill, December 2003

1EP5: Correction of Emergency Preparedness Weaknesses and Deficiencies

Quarterly Self Assessment Report, Fourth Quarter 2003

Quarterly Self Assessment Report, First Quarter 2004

Quarterly Self Assessment Report, LO-ALO-C-2004-145

Biennial Roll-Up Report, Second and Third Quarters 2004

Quarterly Self Assessment Report, Fourth Quarter 2004

Peer Group Assessment, November 17, 2003

Peer Group Assessment, 2004 Dress Rehearsal Exercise

Peer Group Assessment, 2004 Biennial Evaluated Exercise

EP 2003-0064, Full Scale Drill, November 5, 2003

EP 2004-0037, Full Scale Drill, September 15, 2004

EP 2004-0045, Full Scale Drill, October 20, 2004

EP 2004-0053, Full Scale Drill, November 17, 2004

EP 2005-0011, Full Scale Drill, June 1, 2005

EP 2004-0050, Environmental Sampling Drill, November 19, 2004

EP 2004-0051, PASS Drill, December 1, 2004

4OA1: Performance Indicator Verification

EPIP 1903.011, "Emergency Response/Notifications," Attachment 6, "Protective Actions for

General Emergency," Revision 28-00-0

Drill Schedule, 2004

Drill Schedule, 2005

Entergy Nuclear South EP Exercise and Drill Guide, October 2001

Desk Guide EP-006, "Drill/Exercise Manual Addendum," April 2005, Revision 2

Attachment 1

A-12

LIST OF ACRONYMS

ANO

Arkansas Nuclear One

CAP

corrective action program

CEA

control element assembly

CFR

Code of Federal Regulations

CR

condition report

EFW

emergency feedwater

ER

engineering request

ERV

electromatic relief valve

GPD

gallons per day

HELB

high energy line break

HPI

high pressure injection

HPSI

high pressure safety injection

I&C

instrumentation and control

ICS

integrated control system

LER

licensee event report

MC

manual chapter

NCV

noncited violation

NFPA

National Fire Protection Association

SG

steam generator

SSC

structure, system, and component

TI

temporary instruction

URI

unresolved item

Attachment 2

A2-1

ATTACHMENT 2

PHASE 3 EVALUATION, DAMAGED REACTOR COOLANT PUMP SEAL ARKANSAS

NUCLEAR ONE, UNIT 2