ML042080530

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IR 05000271-04-003, on 04/01/04 Through 06/30/04, for Vermont Yankee Nuclear Power Station; Refueling and Outage Activities
ML042080530
Person / Time
Site: Vermont Yankee File:NorthStar Vermont Yankee icon.png
Issue date: 07/26/2004
From: Anderson C
NRC/RGN-I/DRP/PB5
To: Thayer J
Entergy Nuclear Operations
References
FOIA/PA-2005-0031 IR-04-003
Download: ML042080530 (36)


See also: IR 05000271/2004003

Text

July 26, 2004

Mr. Jay K. Thayer

Site Vice President

Entergy Nuclear Operations, Inc.

Vermont Yankee Nuclear Power Station

P.O. Box 0500

185 Old Ferry Road

Brattleboro, VT 05302-0500

SUBJECT:

VERMONT YANKEE NUCLEAR POWER STATION - NRC INTEGRATED

INSPECTION REPORT 05000271/2004003

Dear Mr. Thayer:

On June 30, 2004, the US Nuclear Regulatory Commission (NRC) completed an inspection at

your Vermont Yankee Nuclear Power Station (VY). The enclosed report documents the

inspection findings which were discussed on July 12, 2004, with members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents one finding of very low safety significance (Green) which was also

determined to involve a violation of NRC requirements. Because of the very low safety

significance and because the finding was entered into your corrective actions program, the

NRC is treating it as a non-cited violation (NCV), consistent with Section VI.A of the NRCs

Enforcement Policy. If you contest this non-cited violation, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear

Regulatory Commission, ATTN.: Document Control Desk, Washington, D.C. 20555-0001; with

copies to the Regional Administrator Region I; the Director, Office of Enforcement, United

States Nuclear Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident

Inspector at the Vermont Yankee Nuclear Power Station.

Jay K. Thayer

2

In accordance with 10 CFR 2.390 of the NRCs "Rules of Practice," a copy of this letter, its

enclosure, and your response (if any) will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Clifford J. Anderson, Chief

Projects Branch 5

Division of Reactor Projects

Docket No.

50-271

License No.

DPR-28

Enclosure:

Inspection Report 05000271/2004003

w/Attachment: Supplemental Information

Docket No. 50-271

License No. DPR-28

Jay K. Thayer

3

cc w/encl:

M. R. Kansler, President, Entergy Nuclear Operations, Inc.

G. J. Taylor, Chief Executive Officer, Entergy Operations

J. T. Herron, Senior Vice President and Chief Operating Officer

D. L. Pace, Vice President, Engineering

B. OGrady, Vice President, Operations Support

J. M. DeVincentis, Manager, Licensing, Vermont Yankee Nuclear Power Station

Operating Experience Coordinator - Vermont Yankee Nuclear Power Station

J. F. McCann, Director, Nuclear Safety Assurance

M. J. Colomb, Director of Oversight, Entergy Nuclear Operations, Inc.

J. M. Fulton, Assistant General Counsel, Entergy Nuclear Operations, Inc.

S. Lousteau, Treasury Department, Entergy Services, Inc.

Administrator, Bureau of Radiological Health, State of New Hampshire

Chief, Safety Unit, Office of the Attorney General, Commonwealth of Mass.

D. R. Lewis, Esquire, Shaw, Pittman, Potts & Trowbridge

G. D. Bisbee, Esquire, Deputy Attorney General, Environmental Protection

Bureau

J. Block, Esquire

D. Katz, Citizens Awareness Network (CAN)

M. Daley, New England Coalition on Nuclear Pollution, Inc. (NECNP)

R. Shadis, New England Coalition Staff

C. McCombs, Commonwealth of Massachusetts, SLO Designee

G. Sachs, President/Staff Person, c/o Stopthesale

J. Sniezek, PWR SRC Consultant

R. Toole, PWR SRC Consultant

J. P. Matteau, Executive Director, Windham Regional Commission

State of New Hampshire, SLO Designee

State of Vermont, SLO Designee

Jay K. Thayer

4

Distribution w/encl:

H. Miller, RA/J. Wiggins, DRA (1)

C. Anderson, DRP

D. Florek, DRP

D. Pelton, Senior Resident Inspector

C. Miller, RI EDO Coordinator

J. Clifford, NRR

R. Ennis, PM, NRR

D. Skay, Backup PM, NRR

Region I Docket Room (with concurrences)

DOCUMENT NAME:C:\\ORPCheckout\\FileNET\\ML042080530.wpd

After declaring this document An Official Agency Record it will/will not be released to the Public.

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE RI:DRP

RI:DRP

RI:DRP

NAME

Pelton/CJA for

Florek/CJA for

Anderson/CJA

DATE

07/26/04

07/26/04

07/26/04

OFFICIAL RECORD COPY

Enclosure

i

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No.

50-271

Licensee No.

DPR-28

Report No.

05000271/2004003

Licensee:

Entergy Nuclear Vermont Yankee, LLC

Facility:

Vermont Yankee Nuclear Power Station

Location:

320 Governor Hunt Road

Vernon, Vermont

05354-9766

Dates:

April 1, 2004 - June 30, 2004

Inspectors:

David L. Pelton, Senior Resident Inspector

Beth E. Sienel, Resident Inspector

E. Harold Gray, Senior Reactor Inspector

Todd J. Jackson, Senior Project Engineer

James D. Noggle, Senior Health Physicist

Larry L. Scholl, Senior Reactor Inspector

Keith A. Young, Senior Reactor Inspector

Amar C. Patel, Reactor Inspector

Jennifer A. Bobiak, Reactor Inspector

Thomas P. Sicola, Reactor Inspector

Approved by:

Clifford J. Anderson, Chief

Projects Branch 5

Division of Reactor Projects

Enclosure

ii

TABLE OF CONTENTS

SUMMARY OF FINDINGS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . iii

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R01

Adverse Weather . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R02

Evaluations of Changes, Tests, or Experiments . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R04

Equipment Alignments . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2

1R05

Fire Protection

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R06

Flood Protection Measures . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R08

Inservice Inspection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R11

Licensed Operator Requalification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 5

1R12

Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R13

Maintenance Risk Assessment and Emergent Work Evaluation . . . . . . . . . . . . 6

1R14

Personnel Performance During Non-routine Plant Evolutions . . . . . . . . . . . . . . 7

1R15

Operability Evaluations

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R16

Operator Workarounds . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 8

1R17

Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 9

1R19

Post Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R20

Refueling and Outage Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 10

1R22

Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 15

1R23

Temporary Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

1EP6

Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

2OS1 Access Control to Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . 17

2OS2 ALARA Planning and Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

OTHER ACTIVITIES (OA) . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . 18

4OA3 Event Followup

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

4OA5 Other Activities . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

4OA6 Meetings, including Exit . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

SUPPLEMENTAL INFORMATION . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

KEY POINTS OF CONTACT . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED . . . . . . . . . . . . . . . . . . . . . . . . . . . A-1

LIST OF DOCUMENTS REVIEWED

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-2

LIST OF ACRONYMS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . A-6

Enclosure

iii

SUMMARY OF FINDINGS

IR 05000271/2004003; 04/01/04 - 06/30/04; Vermont Yankee Nuclear Power Station; Refueling

and Outage Activities.

This report covered a 13-week period of baseline inspection conducted by resident inspectors.

Additionally, announced inspections were performed by regional inspectors in the areas of

occupational radiation protection; evaluations of changes, tests, and experiments; in-service

inspections; and permanent plant modifications. One Green non-cited violation (NCV) was

identified. The significance of most findings is indicated by their color (Green, White, Yellow,

Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination Process

(SDP). Findings for which the SDP does not apply may be Green or be assigned a severity

level after NRC management review. The NRC's program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process,"

Revision 3, dated July 2000.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Barrier Integrity

(Green) A self-revealing, non-cited violation (NCV) of 10 CFR 50 Criterion XVI was

identified in that Entergy personnel did not develop effective corrective actions to

prevent recurrence following a 2001 event wherein control room operators did not verify

a suction path existed prior to starting the residual heat removal (RHR) system pump

being used to support shutdown cooling (SDC) operations which caused the pump to

trip. On April 10, 2004, an identical event occurred and again resulted in a trip of the

RHR pump being used to support SDC operations.

The finding is greater than minor since it is associated with the Fuel Cladding

Configuration Control Attribute of the Barrier Integrity Cornerstone and because it

affects the associated Cornerstone objective. The inspectors conducted a SDP Phase 1

screening of the finding in accordance with IMC 0609, Appendix G, Shutdown

Operations Significance Determination Process [SDP]. In accordance with the SDP,

the inspectors determined that the finding was of very low safety significance (Green)

since the RHR pump was restarted within 15 minutes of being tripped and an adequate

SDC thermal margin was maintained as demonstrated by a calculated reactor coolant

system (RCS) time-to-boil of greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

A contributing cause of this finding is related to the Cross-Cutting area of Problem

Identification and Resolution. As stated above, Entergy personnel did not develop

effective corrective actions to prevent recurrence following a 2001 event wherein control

room operators did not verify a suction path existed prior to starting the RHR system

pump being used to support SDC operations which caused the pump to trip. Entergys

corrective actions relied on the operators skill to verify a suction path was open prior to

restarting the RHR pump rather than proceduralize the step. As a result, an identical

event occurred in April 2004 again resulting in a trip of the RHR pump being used to

support SDC operations. (Section 4OA3.1)

Summary of Findings (contd)

Enclosure

iv

B.

Licensee Identified Findings

None.

Enclosure

REPORT DETAILS

Summary of Plant Status

Vermont Yankee Nuclear Power Station entered the inspection period at or near full power.

The reactor was shutdown on April 3, 2004, in support of planned refueling outage (RFO) 24.

Reactor startup activities began on May 3, 2004, following the completion of RFO 24. The

reactor was returned to full power operation on May 8, 2004. On June 18, 2004, an automatic reactor scram occurred as a result of a turbine trip following multiple faults-to-ground on the 22

kilovolt (KV) electrical system. The reactor remained shutdown for the rest of the inspection

period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01

Adverse Weather (71111.01)

a.

Inspection Scope (one sample)

The inspectors reviewed measures established by Entergy for the restoration from cold

weather operations. The inspectors reviewed Vermont Yankee Operating Procedure

(OP) 2196, Preparations for Cold Weather Operations, Form VYOPF 2196.02, Cold

Weather Restoration Operations Checklist, discussed the completion of items with

operations personnel to confirm the items on the checklist had been completed or were

appropriately tracked for completion, and independently walked down portions of the

plant to verify selected actions to restore from cold weather operations had been

completed appropriately.

b.

Findings

No findings of significance were identified.

1R02

Evaluations of Changes, Tests, or Experiments (71111.02)

a.

Inspection Scope (eight samples)

The inspectors reviewed the 10 CFR 50.59 safety evaluations or screening evaluations

associated with plant modifications being installed during the current refueling outage to

support a proposed power uprate. The inspectors assessed the adequacy of the safety

evaluations through interviews with the cognizant plant staff and review of supporting

documentation to verify the changes were performed in accordance with 10 CFR 50.59

and when required, NRC approval was obtained prior to implementation. The inspectors

also reviewed a sample of changes the licensee had evaluated (using a screening

process) and determined to be outside of the scope of 10 CFR 50.59, therefore not

requiring a full safety evaluation. The inspectors performed this review to determine if

Entergy conclusions with respect to 10 CFR 50.59 applicability were appropriate. A

listing of the modifications for which associated safety evaluations, safety evaluation

2

Enclosure

screenings, and other documents were reviewed is provided in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

1R04

Equipment Alignments

1.

Complete Equipment Alignment (71111.04S)

a.

Inspection Scope (one sample)

The inspectors performed a complete equipment alignment inspection of the accessible

portions of the core spray (CS) system. The inspectors walked down the CS system,

both inside and outside of the primary containment, and compared actual equipment

alignment to approved piping and instrumentation diagrams, operating procedure

lineups, the Vermont Yankee updated final safety analysis report (UFSAR), and the

Vermont Yankee design basis document (DBD). The inspectors observed valve

positions, the availability of power supplies, and the general condition of selected

components to verify there were no unidentified deficiencies. The inspectors also

confirmed that licensee-identified equipment problems had been entered into the

corrective actions program.

b.

Findings

No findings of significance were identified.

2.

Partial Equipment Alignments (71111.04)

a.

Inspection Scope (four samples)

The inspectors performed four partial system walkdowns of risk significant systems to

verify system alignment and to identify any discrepancies that would impact system

operability. Observed plant conditions were compared with the standby alignment of

equipment specified in the licensees system operating procedures and drawings. The

inspectors also observed valve positions, the availability of power supplies, and the

general condition of selected components to verify there were no obvious deficiencies.

The inspectors verified the alignment of the following systems:



The spent fuel pool (SFP) cooling system while the A train of the residual heat

removal (RHR) system was unavailable to support shutdown cooling on June 6,

2004;



The B train of the standby gas treatment (SBGT) system during planned

maintenance on the A SBGT fan on June 7, 2004;

3

Enclosure



The A train of SBGT during planned instrument calibrations on the B train of

SBGT on June 8; and



The emergency diesel generators (EDGs), start-up transformers, the diesel oil

storage tank (DOST) following the main transformer fire on June 18, 2004.

b.

Findings

No findings of significance were identified.

1R05

Fire Protection (71111.05Q)

a.

Inspection Scope (nine samples)

The inspectors identified fire areas important to plant risk based on a review of Entergys

the Vermont Yankee Safe Shutdown Capability Analysis, the Fire Hazards Analysis, and

the individual plant evaluation of external events (IPEEE). The inspectors toured plant

areas important to safety in order to verify the suitability of Entergys control of transient

combustibles and ignition sources, and the material condition and operational status of

fire protection systems, equipment, and barriers. The following fire areas were

inspected:



Reactor building, 252 foot elevation-S1 cable trays (CFZ-3/4);



Reactor building, 252 foot elevation-S2 cable trays (CFZ-3/4);



Reactor building, 252 foot elevation, North (FZ RB3);



Reactor building, 252 foot elevation, South (FZ RB4);



Reactor building, 280 foot elevation, Recirc MG set area (SZ RB-MG);



Turbine building, all elevations (FA TB);



Torus room, 213 foot elevation, North (FZ RB1);



Torus room, 213 foot elevation, South (FZ RB2);



345 KV relay house.

b.

Findings

No findings of significance were identified.

1R06

Flood Protection Measures (71111.06)

a.

Inspection Scope (one sample)

The inspectors reviewed Entergys established flood protection barriers and procedures

for coping with internal flooding in the EDG rooms including Vermont Yankee Off-

Normal Procedure (ON) 3148, Loss of Service Water; and ON 3158, Reactor Building

High Area Temperature/Water Level. The inspectors reviewed internal flooding

information contained in Entergys IPEEE, in the UFSAR, and in the Internal Flooding

DBD as it related to the EDG rooms. Finally, the inspectors performed walk-downs of

flood vulnerable portions of the EDG rooms to ensure equipment and structures needed

4

Enclosure

to mitigate an internal flooding event were as described in the IPEEE and the DBD.

Additionally, the inspectors reviewed condition reports (CRs) related to internal flooding

and the EDG rooms to ensure identified problems were properly addressed for

resolution.

b.

Findings

No findings of significance were identified.

1R08

Inservice Inspection (71111.08G)

a.

Inspection Scope (four samples)

The inspectors assessed the inservice inspection (ISI) activities using the criteria

specified in the American Society of Mechanical Engineers (ASME) Boiler and Pressure

Vessel Code,Section XI.

The inspectors observed selected in-process non-destructive examination (NDE)

activities, reviewed documentation and interviewed personnel to verify that the activities

were performed in accordance with the ASME Boiler and Pressure Vessel Code Section

XI requirements. The sample selection was based on the inspection procedure

objectives and risk priority of those components and systems where degradation would

result in a significant increase in risk of core damage. The inspectors reviewed a

sample of condition reports and quality assurance audit reports to assess the licensees

effectiveness in problem identification and resolution. The specific ISI activities selected

for review included:

Observation of the ultrasonic testing (UT) manual technique, UT procedure, weld

overlay calibration test block, and performance of pre and post examination

calibration for UT of the CS system N5A safe-end to nozzle structural weld

overlay;

Review of the computer based UT procedure and observation of its application

for the reactor vessel welds and the eddy current (ET) examination method to

quantify clad crack shadowing of volumetric vessel weld examinations and the

results for the reactor vessel flange-to-vessel weld;

Observation of the UT examination of a pre-existing reactor vessel weld

indication for verification that the indication was appropriately characterized and

had not increased in dimension since the previous examination;

Review of CS system sparger video-visual examination records;

Review of the inspection scope expansion and disposition of two small linear

indications on a standby liquid control system socket weld (SL11-F12); and

Review of the reactor vessel internals project (BWRVIP-03 Rev 6) procedure

and observation of some of the initial visual examinations.

In response to Entergys extended power up-rate request and recent industry operating

experience, the inspectors observed portions of the steam dryer visual testing (VT) type

5

Enclosure

1 and type 3 examinations and reviewed the documented examination reports. The

examination reports documented that cracks were identified on both the internal and

external surfaces of the steam dryer. The inspectors reviewed Entergys corrective

actions for these indications to ensure that the actions were appropriate. Specifically,

the inspectors reviewed the weld repair activities for the two cracks identified on the

external surface of the steam dryer. The inspectors also reviewed the vendor technical

reports which justified operation for the next operating cycle at the current maximum

licensed power level without repair of the indications identified on internal portions of the

steam dryer.

b.

Findings

No findings of significance were identified.

1R11

Licensed Operator Requalification (71111.11Q)

a.

Inspection Scope (one sample)

The inspectors observed simulator examinations for one operating crew to assess the

performance of the licensed operators and the ability of Entergys Training Department

staff to evaluate licensed operator performance. Operating crew performance was

evaluated during a simulated main steam line break inside the drywell coincident with a

loss of normal power. The inspectors evaluated the crews performance in the areas of:

Clarity and formality of communications;

Ability to take timely actions;

Prioritization, interpretation, and verification of alarms;

Procedure use;

Control board manipulations;

Oversight and direction from supervisors; and

Group dynamics.

Crew performance in these areas was compared to Entergy management expectations

and guidelines as presented in the following documents:

Vermont Yankee Administrative Procedure (AP) 0151, Responsibilities and

Authorities of Operations Department Personnel;

AP 0153, Operations Department Communication and Log Maintenance; and

Vermont Yankee Department Procedure (DP) 0166, Operations Department

Standards.

The inspectors verified that the crew completed the critical tasks listed in the associated

simulator evaluation guide (SEG). The inspectors also compared simulator

configurations with actual control board configurations. For any weaknesses identified,

the inspectors observed the licensee evaluators to verify that they also noted the issues

to be discussed with the crew.

6

Enclosure

b.

Findings

No findings of significance were identified.

1R12

Maintenance Effectiveness (71111.12Q)

a.

Inspection Scope (three samples)

The inspectors performed three issue/problem-oriented inspections of actions taken by

Entergy in response to the following issues:

As-found local leakage rate testing (LLRT) failures of the high pressure coolant

injection (HPCI) turbine exhaust vacuum breakers;

Repeat failures of the C residual heat removal service water (RHRSW) system

pump motor cooling solenoid valve; and

A trend of unavailability associated with the diesel-driven fire pump.

The inspectors reviewed applicable system maintenance rule scoping documents,

system health reports, corrective actions taken in response to the equipment problems,

maintenance rule functional failure determinations, and applicable a(1) action plans. In

addition, the issues were discussed with the responsible engineer.

b.

Findings

No findings of significance were identified.

1R13

Maintenance Risk Assessment and Emergent Work Evaluation (71111.13)

a.

Inspection Scope (seven samples)

The inspectors evaluated on-line and outage risk management for six planned and one

emergent maintenance activities. The inspectors reviewed maintenance risk

evaluations, work schedules, recent corrective actions, and control room logs to verify

that other concurrent or emergent maintenance activities did not significantly increase

plant risk. The inspectors also compared these items and activities to requirements

listed in Vermont Yankee AP 0125, "Equipment Release"; AP 0172, "Work Schedule

Risk Management - Online"; and AP 0173, Work Schedule Risk Management -

Outage. The inspectors reviewed the following work activities:

Online Risk:

Planned maintenance on the service water (SW) system supply to turbine the

building valve SW-19B breaker, resulting in Yellow online risk;

Planned maintenance on the A train of SBGT; and

Emergent work to implement minor modification on average power range

monitors (APRMs), resulting in a 1/2 scram condition and Yellow online risk.

7

Enclosure

Outage Risk:

Planned realignment and testing of offsite electrical power via the delayed

backfeed through the auxiliary and main transformers;

Planned maintenance resulting in 345 KV 340 line and 1T breaker being out of

service;

Portions of planned maintenance on electrical buses 2, 4, and 9; and

Planned performance of reactor pressure vessel leakage testing; considered by

Entergy to be a high risk evolution.

b.

Findings

No findings of significance were identified.

1R14

Personnel Performance During Non-routine Plant Evolutions (71111.14)

a.

Inspection Scope (two samples)

The inspectors assessed the control room operator performance during the following

two non-routine evolutions:

Entry into emergency operating procedure (EOP) 3, Primary Containment

Control, due to average torus temperature exceeding 90 degrees during HPCI

system testing on May 26, 2004; and

Reactor scram following the main transformer fire on June 18, 2004.

Specifically, the adequacy of personnel performance, procedure compliance, and use of

the corrective action process were evaluated against the requirements and expectations

contained in technical specifications and the following station procedures, as applicable:

AP 0151, Responsibilities and Authorities of Operations Department Personnel;

AP 0153, Operations Department Communication and Log Maintenance;

Vermont Yankee DP 0166, Operations Department Standards;

Vermont Yankee OP 105, Reactor Operations; and

OP 2124, Residual Heat Removal System.

b.

Findings

No findings of significance were identified.

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope (five samples)

8

Enclosure

The inspectors reviewed five operability determinations prepared by the licensee. The

inspectors evaluated the selected operability determinations against the requirements

and guidance contained in NRC Generic Letter 91-18, Resolution of Degraded and

Nonconforming Conditions, as well as procedures AP 0167, Operability

Determinations, and ENN-OP-104, Operability Determinations. The inspectors

verified the adequacy of the following evaluations of degraded or non-conforming

conditions:

Flow noise from the C RHR system pump discharge orifice;

Broken 4 KV breaker driving pawl;

Missing clam shell from the control rod drive housing support system;

Apparent non-conservative flow-biased scram setpoints; and

Incomplete NDE for lifting and handling gear.

b.

Findings

No findings of significance were identified.

1R16

Operator Workarounds (71111.16)

a.

Inspection Scope (one sample)

The inspectors reviewed the cumulative effect of operator workarounds on the reliability,

availability, and potential mis-operation of systems and the potential to affect the ability

of operators to respond to plant transients and events. The inspectors reviewed

identified operator burdens, control room deficiencies, disabled or illuminated control

room alarms, and component deviations and discussed them with responsible

operations personnel to ensure they were appropriately categorized and tracked for

resolution. In addition, in-plant and control room tours were performed to identify any

workarounds not previously identified in accordance with procure DP 0166, Operations

Department Standards.

b.

Findings

No findings of significance were identified.

9

Enclosure

1R17

Permanent Plant Modifications

1.

Annual Review (71111.17A)

a.

Inspection Scope (one sample)

The inspectors performed an annual review of a permanent plant modification involving

the installation of an additional main steam safety valve installed during RFO 24. The

inspectors reviewed this modification to verify that the design bases, licensing bases,

and performance capability of risk significant structures, systems, and components

(SSCs) had not been degraded through the modifications. The review evaluated the

impact of the modification on power operation at the current licensed power level and

potential future operation at an increased power rating. This plant modification was

selected for review based on risk insights for the plant and included SSCs associated

with the initiating events, mitigating systems and barrier integrity cornerstones. The

inspection included a walkdown of the modification, interviews with plant staff, and the

review of applicable documents including procedures, Vermont Yankee Design

Calculation (VYDC) 2003-013, the modification package, engineering evaluations,

drawings, corrective action documents, the UFSAR and Technical Specifications. The

inspectors verified that selected attributes were consistent with the current design and

licensing bases. These attributes included component safety classification, energy

requirements supplied by supporting systems, instrument set-points, and control system

interfaces. Design assumptions were reviewed to verify that they were technically

appropriate and consistent with the UFSAR. The inspectors verified that selected

procedures, calculations and the UFSAR were properly updated with revised design

information and operating guidance. The inspectors also verified that the as-built

configuration was accurately reflected in the design documentation and that post-

modification testing was appropriate.

b.

Findings

No findings of significance were identified.

2.

Biennial Review (71111.17B)

a.

Inspection Scope (six samples)

The inspectors performed a biennial review of selected plant modifications that were

being installed during RFO 24. The modifications support a proposed power uprate that

is currently under review by the Office of Nuclear Reactor Regulation (NRR). The

inspectors reviewed the modifications to verify that the design bases, licensing bases,

and performance capability of risk significant SSCs had not been degraded through the

modifications. The reviews evaluated the impact of the modifications on power

operation at the current licensed power level and potential future operation at an

increased power rating. Plant modifications were selected for review based on risk

insights for the plant and included SSCs associated with the initiating events, mitigating

10

Enclosure

systems and barrier integrity cornerstones. The inspection included walkdowns of

selected plant systems and components, interviews with plant staff, and the review of

applicable documents including procedures, calculations, modification packages,

engineering evaluations, drawings, corrective action documents, the UFSAR and

Technical Specifications. The inspectors verified that selected attributes were

consistent with the current design and licensing bases. These attributes included

component safety classification, energy requirements supplied by supporting systems,

instrument set-points, and control system interfaces. Design assumptions were

reviewed to verify that they were technically appropriate and consistent with the UFSAR.

The inspectors verified that selected procedures, calculations and the UFSAR were

properly updated with revised design information and operating guidance. The

inspectors also verified that the as-built configuration was accurately reflected in the

design documentation and that post-modification testing was appropriate. A listing of

documents reviewed is provided in the Attachment to this report.

b.

Findings

No findings of significance were identified.

1R19

Post Maintenance Testing (71111.19)

a.

Inspection Scope (three samples)

The inspectors reviewed completed documentation for three post-maintenance test

(PMT) activities to verify the test data met the required acceptance criteria contained in

the licensees Technical Specifications, UFSAR, and in-service testing program, and

that the PMT was adequate to verify system operability and functional capability

following maintenance. The inspectors reviewed the PMTs performed after the following

maintenance activities:

Installation of low feedwater pump suction pressure trip modifications in

accordance with minor modification (MM) 2003-015;

APRM flow control trip reference card replacement in accordance with MM 2003-

028; and

Disassembly and repair of HPCI turbine exhaust check valve V23-3 following

failed as-found LLRT.

The inspectors verified that systems were properly restored following testing and that

discrepancies were appropriately documented in the corrective action process. The

inspectors also discussed the PMT results with the responsible engineers.

b.

Findings

No findings of significance were identified.

1R20

Refueling and Outage Activities (71111.20)

11

Enclosure

1.

Refueling Outage (RFO) 24

a.

Inspection Scope (one sample)

The inspectors evaluated the following outage activities to verify that Entergy considered

risk when developing outage schedules; that Entergy adhered to administrative risk

reduction methodologies for plant configuration control; and to ensure that Entergy

adhered to their operating license, Technical Specification requirements, and approved

procedures:

Review of the Outage Plan - The inspectors reviewed the RFO 24 shutdown risk

assessment to verify that Entergy addressed the outages impact on

defense-in-depth for the five shutdown critical safety functions; electrical power

availability, inventory control, decay heat removal, reactivity control, and

containment. Adequate defense-in-depth was verified for each safety function

and / or where redundancy was limited or not available, the existence of

appropriate planned contingencies, to minimize the overall risk, was verified.

Consideration of operational experience was also verified. The daily risk

up-date, accounting for schedule changes and unplanned activities were also

periodically reviewed;

Monitoring of Shutdown Activities - The inspectors observed the shutdown of the

reactor plant including reactor plant cooldown and transition to shutdown cooling

operations. As soon as practical following the shutdown, the inspectors

performed walkdowns of the primary containment;

Electrical Power - The inspectors reviewed the status and configuration of

safety-related buses throughout RFO 24. The inspectors ensured the electrical

lineups met the requirements of Technical Specification and the outage risk

control plan. The inspectors performed frequent walkdowns of affected portions

of the electrical plant including startup transformers, the auxiliary transformer,

and the emergency diesel generators;

Decay heat removal (DHR) System Monitoring - The inspectors monitored decay

heat removal status on a daily basis. Monitoring included daily reviews of

residual heat removal system alignment, reviews of spent fuel pool cooling

system alignment, and reviews of reactor coolant system (RCS) time-to-boil

calculations and results;

Inventory Control - The inspectors performed daily RCS inventory control reviews

including reviews of available injection systems and flow paths to ensure

consistency with the outage risk plan. The inspectors also ensured that

operators maintained reactor vessel and/or refueling cavity levels within

established ranges;

Reactivity Control - The inspectors observed reactivity management actions

taken by control room operators during refueling evolutions including procedure

place keeping, communications with refueling floor personnel, the monitoring of

source range nuclear instrumentation, and the monitoring of individual control

rod positions;

12

Enclosure

Containment Closure - The inspectors performed a torus internal cleanliness

walkdown following completion of outage activities. The inspectors performed a

primary containment closeout walkdown prior to final containment closure.

Finally, the inspectors ensured secondary containment was maintained as

required by Technical Specifications;

Refueling Activities - The inspectors observed portions of refueling operations,

including fuel handling and accounting in the reactor vessel and spent fuel pool.

The inspectors also performed an independent core reload verification of

approximately 34% of the core; and

Heatup and Startup Activities - The inspectors observed portions of the heatup

and startup of the reactor plant following the completion of RFO24.

The inspectors also verified that Entergy identified problems related to refueling

activities and entered them into their corrective actions program.

b.

Findings

Introduction: A very low safety significance (Green), self-revealing, non-cited violation

(NCV) of 10 CFR 50 Criterion XVI was identified in that Entergy personnel did not

develop effective corrective actions to prevent recurrence following a 2001 event

wherein control room operators did not verify a suction path existed prior to starting a

residual heat removal (RHR) system pump being used to support shutdown cooling

(SDC) operations which caused the pump to trip. On April 10, 2004, an identical event

occurred and again resulted in a trip of the RHR pump being used to support SDC

operations.

Description: On April 10, 2004, control room operators realigned vital alternating current

(AC) power from its normal power supply to the backup power supply to support planned

maintenance on a vital AC motor generator. The reactor plant was in the refueling

mode of operation at that time. In preparation for the vital AC realignment, operators

temporarily secured the RHR system, which was running in the SDC mode of operation.

One of the automatic actions that occurred during the vital AC alignment was the

closure of the RHR pump suction valve V10-17 from a Group 4 containment isolation

signal. Once the realignment of the vital AC power was completed, operators reset the

expected partial Group 4 containment isolation signal, but did not recognize that this

partial Group 4 containment isolation signal resulted in the closure of RHR system valve

V10-17, isolating the suction path used for RHR system support of SDC. Operators

subsequently attempted to reinitiate the RHR system in accordance with Vermont

Yankee Operating Procedure (OP) 2124, Residual Heat Removal System, Section J,

Short Term Shutdown Cooling Shutdown and Startup. When the B RHR pump was

started, the pumps breaker immediately tripped open due to a designed electrical

interlock requiring valve V10-17 to be open to provide a suction path for the RHR

system. Operators investigated the cause of the pump breaker trip, identified that no

suction path existed since valve V10-17 had closed, re-opened valve V10-17, and

successfully restarted the B RHR pump within 15 minutes of the breaker trip.

13

Enclosure

SDC thermal margin was maintained throughout this event via continued operation of

the spent fuel pool cooling system along with a calculated RCS time-to-boil value of

greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

In the apparent cause report for this event, Entergy identified that a nearly identical

event had occurred during a refueling outage in May 2001. At that time, operators had

performed a planned realignment of the vital AC power but did not recognize that valve

V10-17 had closed which resulted in a trip of the C RHR pump breaker when operators

attempted to reinitiate the RHR system. Entergy documented this previous event in

event report (ER) 2001-01228. Corrective actions assigned at that time included

discussions at shift supervisor meetings and the counseling of involved operators. In

the apparent cause report, Entergy also concluded that the corrective actions taken to

address the May 2001 event were insufficient to have prevented recurrence of the

nearly identical April 2004 event. Specifically, no corrective actions were assigned to

address the fact that OP 2124, Section J, did not specifically require operators to verify

an adequate RHR system flow path to and from the reactor existed prior to reinitiating

system operation.

Analysis: The performance deficiency associated with this finding is that Entergy

personnel did not assign effective corrective actions to prevent recurrence as required

by VY Administrative Procedure 0009 following a May 2001 trip of the C RHR pump

which occurred when operations did not recognize that RHR system valve V10-17 had

gone closed during a realignment of vital AC power. As a result, a similar event

occurred in April of 2004 involving a trip of the B RHR pump resulting from operators

again failing to recognize the closure of valve V10-17 during a realignment of vital AC

power. The finding is greater than minor since it is associated with the Fuel Cladding

Configuration Control Attribute of the Barrier Integrity Cornerstone and because it

affects the associated Cornerstone objective. Specifically, the April 2004 trip of the B

RHR pump, used to support SDC operations, reduced the assurance that the fuel

cladding would protect the public from radio nuclide releases caused by accidents or

events. The inspectors conducted a SDP Phase 1 screening of the finding in

accordance with IMC 0609, Appendix G, Shutdown Operations Significance

Determination Process [SDP]. The inspectors determined that Entergy did not meet

Item I.C. of Table 1, BWR [Boiling Water Reactor] Refueling Operation with RCS Level

> 23' since the finding resulted in Entergy not having at least one RHR loop operating

to support SDC. However, the inspectors also determined that the finding did not

degrade Entergys ability to recover SDC since the B RHR pump was restarted within

15 minutes of being tripped and an adequate thermal margin was maintained via a

calculated RCS time-to-boil of greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Therefore, in accordance with

IMC 0609, Appendix G, the finding was of very low safety significance (Green).

A contributing cause of this finding is related to the Cross-Cutting area of Problem

Identification and Resolution. As stated above, Entergy personnel did not develop

effective corrective actions to prevent recurrence following a 2001 event wherein control

room operators did not verify a suction path existed prior to starting the RHR system

pump being used to support SDC operations which caused the pump to trip. Entergys

corrective actions relied on the operators skill to verify a suction path was open prior to

14

Enclosure

restarting the RHR pump rather than proceduralize the step. As a result, an identical

event occurred in April 2004 again resulting in a trip of the RHR pump being used to

support SDC operations.

Enforcement:

10 CFR 50, Appendix B, Criterion XVI states, in part, that measures shall be established

to assure that conditions adverse to quality are promptly identified and corrected.

Vermont Yankee AP 0009, Event Reports, Revision 12, describes Entergys

requirements for the identification and correction of conditions adverse to quality

including determining the cause(s) of the event and assigning corrective actions that

prevent recurrence. Contrary to the above, in May 2001, Entergy did not assign

effective corrective actions that prevent recurrence following a May 2001 trip of the C

RHR pump which occurred when operators did not recognize that RHR system valve

V10-17 had closed due to an expected partial Group 4 containment isolation during the

realignment of vital AC power. As a result, a similar event occurred in April of 2004

involving the trip of the B RHR pump resulting from operators again failing to recognize

the closure of valve V10-17 during a realignment of vital AC power. Because the finding

is of very low safety significance and has been entered into the licensees Corrective

Actions Program (CR 2004-01005), this violation is being treated as an NCV, consistent

with Section VI.A of the NRC Enforcement Policy: NCV 0500271/2004003-01,

Ineffective Corrective Actions Assigned Following a May 2001 Trip of the C RHR

System Pump During SDC Operation.

2.

Forced Outage Following the Main Transformer Fire of June 18, 2004.

a.

Inspection Scope (partial sample)

The inspectors evaluated the following forced outage activities to verify that Entergy

considered risk when developing outage schedules; that Entergy adhered to

administrative risk reduction methodologies for plant configuration control; and to ensure

that Entergy adhered to their operating license, Technical Specification requirements,

and approved procedures:

Review of the Outage Plan - The inspectors reviewed the shutdown risk

assessment to verify that Entergy addressed the outages impact on

defense-in-depth for the five shutdown critical safety functions; electrical power

availability, inventory control, decay heat removal, reactivity control, and

containment. The daily risk up-date, accounting for schedule changes and

unplanned activities were also periodically reviewed;

Monitoring of Shutdown Activities - The inspectors observed the shutdown of the

reactor plant including reactor plant cooldown activities and transition to

shutdown cooling operations. As soon as practical following the shutdown, the

inspectors performed walkdowns of the primary containment;

DHR System Monitoring - The inspectors monitored decay heat removal on a

daily basis. Monitoring included daily reviews of residual heat removal system

15

Enclosure

alignment, reviews of spent fuel pool cooling system alignment, and reviews of

RCS time-to-boil calculations and results; and

Inventory Control - The inspectors performed daily RCS inventory control reviews

including reviews of available injection systems and flow paths to ensure

consistency with the outage risk plan. The inspectors also ensured that

operators maintained RCS level within established ranges.

The inspectors also verified that Entergy identified problems related to the forced outage

and entered them into their corrective actions program.

b.

Findings

No findings of significance were identified.

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope (eight samples)

The inspectors observed surveillance testing to verify that the test acceptance criteria

specified for each test was consistent with Technical Specification and UFSAR

requirements, was performed in accordance with the written procedure, the test data

was complete and met procedural requirements, and the system was properly returned

to service following testing. The inspectors observed selected pre-job briefs for the test

activities. The inspectors also verified that discrepancies were appropriately

documented in the corrective action program. The inspectors verified that testing in

accordance with the following procedures met the above requirements:

OP 4031, Type B and C Primary Containment Leak Rate Calculations and

Evaluations;

OP 4100, ECCS Integrated Automatic Initiation Test;

OP 4114, Standby Liquid Control [SLC] System Surveillance, Section C, Flow

Test Directly into the Reactor Vessel, and Section I, SLC Explosive Charge

Continuity Check;

OP 4121, Reactor Core Isolation Cooling System Surveillance, Section B,

RCIC Injection Check Valve (RCIC-22) Test;

OP 4142, Vernon Tie and Delayed Access Power Source Backfeed

Surveillance;

OP 4424, Control Rod Scram Testing and Data Reduction, Section B, Single

Rod Scrams Using ERFIS Data Collection;

OP 4430, Reactivity Anomalies/Shutdown Margin Check, Section 1, Strongest

Control Rod Withdrawn Subcritical Check; and

Special Test Procedure (STP) 2003-004, Power Ascension Test Procedure.

b.

Findings

No findings of significance were identified.

16

Enclosure

1R23

Temporary Modifications (71111.23)

a.

Inspection Scope (two samples)

The inspectors reviewed the following temporary modifications (TMs) to ensure that the

modifications did not adversely affect the availability, reliability, or functional capability of

any risk-significant structures, systems, and components:

TM 2003-039, Bottom Head Drain Line Freeze Seal; and

TM 2003-022, Vibration Monitoring Equipment Installation on MS & FW Piping.

The inspectors compared the information in the TM packages to Entergys TM

requirements contained in AP 0020, Control of Temporary and Minor Modifications.

The inspectors also walked down accessible portions of these TMs to verify that

required tags and markings were applied and that the TMs were properly maintained.

The inspectors also reviewed a sample of TM-related problems identified in the

Entergys corrective action program to verify that they had identified and implemented

appropriate corrective actions.

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP6

Drill Evaluation (71114.06)

a.

Inspection Scope (one sample)

On June 17, 2004, the inspectors observed an operating crew evaluate a simulator-

based event using the station emergency action levels (EALs) during licensed operator

requalification training activities. The inspectors discussed the performance

expectations and results with the lead instructor and operations training manager. The

inspectors focused on the ability of licensed operators to perform event classification

and make proper notifications in accordance with the following station procedures and

industry guidance:

AP 0153, Operations Department Communications and Log Maintenance;

AP 0156, Notification of Significant Events;

AP 3125, Emergency Plan Classification and Action Level Scheme;

DP 0093, Emergency Planning Data Management;

OP 3540, Control Room Actions During an Emergency; and

Nuclear Energy Institute (NEI) 99-02, Regulatory Assessment Performance

Indicator Guideline, Revision 2.

b.

Findings

17

Enclosure

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

a.

Scope (fourteen samples)

The inspectors conducted inspections to verify that Entergy was properly implementing

physical, engineering, and administrative controls for access to high radiation areas, and

other radiologically controlled areas, and that workers were adhering to these controls

when working in these areas. Implementation of the access control program was

reviewed against the criteria contained in 10 CFR 20, Technical Specifications, and

approved Entergy procedures. The inspectors conducted independent radiation surveys

and observed work area conditions, reviewed radiation surveys of these areas, and

reviewed electronic dosimetry set points and other exposure controls specified in the

radiation work permits (RWPs) that provided the access control requirements for the

following radiologically significant work activities:

Steam dryer underwater welding modifications;

Drywell shielding installation;

Drywell in-service inspection of core spray nozzle N5A;

Drywell safety relief valve maintenance;

Drywell main steam isolation valve maintenance; and

Feedwater heater replacement modifications

b.

Findings

No findings of significance were identified.

2OS2 ALARA Planning and Controls (71121.02)

Inspection Scope (four samples)

The inspectors reviewed Entergys As Low As Reasonably Achievable (ALARA)

Program performance against the requirements of 10 CFR 20.1101(b). The inspectors

reviewed aspects of the implementation of exposure reduction requirements based on

ALARA planning for the five highest exposure outage tasks. The ALARA-related work

activities observed are listed in Section 2OS1 above. In addition, the following ALARA

inspection activities were conducted:

Independent shielding effectiveness radiation surveys conducted in the drywell;

Observation of closed circuit television equipment and tele-dosimetry use in the

drywell was conducted with respect to drywell remote health physics work

surveillance capability and technical specification requirements; and

18

Enclosure

Feedwater heater bay source term location was reviewed relative to worker

occupancy areas.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES (OA)

4OA1 Performance Indicator Verification (71151)

a.

Inspection Scope (two samples)

The inspectors sampled Entergy submittals for the performance indicators (PIs) listed

below for the period from April 2003 to March 2004. The PI definitions and guidance

contained in NEI 99-02 and AP 0094, NRC Performance Indicator Reporting, were

used to verify the accuracy and completeness of the PI data reported during this period.

Barrier Integrity Cornerstone

Reactor Coolant System Specific Activity; and

Reactor Coolant System Leakage.

The inspectors reviewed selected operator logs, plant process computer data, condition

reports, and monthly operating reports for the period April 1, 2003, through March 31,

2004.

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

1.

Routine Review of Identification and Resolution of Problems

a.

Inspection Scope

The inspectors routinely reviewed issues during baseline inspection activities and plant

status reviews to verify they were being entered into Entergys corrective action system

at an appropriate threshold and that adequate attention was being given to timely

corrective actions. Additionally, in order to identify repetitive equipment failures and/or

specific human performance issues for follow-up, the inspectors performed a daily

screening of items entered into Entergys corrective action program. This review was

accomplished by reviewing selected hard copies of condition reports (a listing of CRs

reviewed is included in the Attachment to this report) and/or by attending daily screening

meetings.

19

Enclosure

b.

Findings

No findings of significance were identified.

2.

Semi-Annual Trend Review

a.

Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

the inspectors performed the semi-annual trend review to identify trends, either licensee

or NRC identified, that might indicate the existence of a more significant safety issue.

Included within the scope of this review were:

CRs generated from January through May 2004;

Corrective maintenance backlog listings from January through May 2004;

The corrective action program 3rd and 4th quarter, 2003 trend report; and

Daily review of main control room operator logs.

b.

Findings

No findings of significance were identified.

3.

Cross-Reference to PI&R Findings Documented Elsewhere

Section 1R20.1 describes a finding wherein Entergy personnel did not develop effective

corrective actions to prevent recurrence following a 2001 event wherein control room

operators did not verify a suction path existed prior to starting the RHR system pump

being used to support SDC operations which caused the pump to trip. Entergys

corrective actions relied on the operators skill to verify a suction path was open prior to

restarting the RHR pump rather than proceduralize the step. As a result, an identical

event occurred in April 2004 again resulting in a trip of the RHR pump being used to

support SDC operations.

4OA3 Event Followup (71153)

1.

Main Transformer Fire and Reactor Plant Scram

a.

Inspection Scope (1 sample)

The inspectors evaluated Entergys response to a main transformer fire and resultant

reactor plant scram that occurred on June 18, 2004. The inspectors immediately

responded to the main control room to observe reactor plant parameters, to evaluate

individual safety system responses, and to evaluate licensed operator responses to the

event. The inspectors evaluated the response of the reactor plant and the licensed

operators against Entergy approved operating procedures, abnormal operating

procedures, and emergency operating procedures. The inspectors evaluated Entergys

classification of the event (i.e., Unusual Event) in accordance with approved EAL

20

Enclosure

procedures to ensure notifications were made to NRC and state/county governments as

required. The inspectors also evaluated the ability of Entergys fire brigade and

automatic fire protection systems to extinguish the main transformer fire in a safe and

timely manner.

The NRC Region I Office dispatched two inspectors, each a specialist in the areas of

electrical and fire protection systems, to assist the resident inspectors with event follow-

up activities. The inspectors monitored Entergys efforts in determining the root cause

of the event; monitored Entergys efforts for the recovery, replacement, and repair of the

effected portions of the 22KV electrical system; and monitored Entergys reactor plant

restart preparation activities.

b.

Findings

Entergy has identified that the root cause of the main transformer fire relates to

weaknesses with the preventive maintenance performed on the 22 KV electrical system.

Because additional information is needed to determine if these issues are more than

minor, they are considered to be an unresolved item (URI) pending completion of the

inspectors review of Entergys root cause analysis: URI 0500271/2004003-02,

Weaknesses Identified with the Preventive Maintenance Performed on the 22 KV

Electrical System Resulted in Main Transformer Fire.

4OA5 Other Activities

1.

Temporary Instruction (TI) 2515/156, Offsite Power System Operational Readiness.

a.

Inspection Scope

The inspectors collected and reviewed information pertaining to the Vermont Yankee

offsite power system as it related to the requirements of 10 CFR 50.65, Requirements

for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants; 10 CFR 50.63, Loss of All Alternating Current Power; offsite power operability; and corrective

actions. The inspectors also reviewed this data against the requirements of 10 CFR 50,

Appendix A, General Design Criterion 17, Electric Power Systems, and the Vermont

Yankee Technical Specifications. This information was forwarded to NRR for further

review. A listing of documents reviewed is included in the Attachment to this report.

b.

Findings

No findings of significance were identified.

4OA6 Meetings, including Exit

Resident Exit

On July 12, 2004, the resident inspectors presented the inspection results to Mr. Kevin

Bronson and members of his staff. The inspectors asked whether any materials

21

Enclosure

examined during the inspection should be considered proprietary. No proprietary

information was identified.

Meeting with the State of Vermont Public Service Board

On June 28, 2004, Region I and NRR staff met with the Vermont State Public Service

Board (PSB) regarding Vermont Yankees request for a 20% extended power uprate.

The NRC staff discussed the NRCs power uprate review process and details regarding

a planned pilot engineering inspection slated for Vermont Yankee in August 2004.

ATTACHMENT: SUPPLEMENTAL INFORMATION

A-1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel:

J. Thayer

Site Vice President

K. Bronson

General Plant Manager

J. Allen

Design Engineering

P. Corbett

Maintenance Manager

J. Dreyfuss

Project Engineering Manager

J. Devincentis Licensing Manager

W. Fadden

Design Engineering

J. Geyster

Radiation Protection Superintendent

D. Giorowall

Programs Supervisor

Dennis Girrior Programs Supervisor

S. Goodwin

Mechanical Design Department Manager

M. Gosekamp Superintendent of Operations Training

M. Hamer

Licensing

D. Johnson

Design Engineering

Dave King

ISI Coordinator

R. Morissette Principal As Low As Reasonably Achievable (ALARA) Engineer

M. Pletcher

Radiation Protection Supervisor - Instruments

P. Rainey,

Design Engineering

B. Renny

Supervisor, Access Authorization

K. Stupak

Technical Training

C. Wamser

Operations Manager

R. Wanczyk

Director of Nuclear Safety

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened and Closed

0500271/2004003-01 NCV

Ineffective Corrective Actions Assigned Following a May

2001 Trip of the C RHR System Pump During SDC

Operation (Section 1R20.1)

Opened

0500271/2004003-02 URI

Weaknesses Identified with the Preventive Maintenance

Performed on the 22 KV Electrical System Resulted in

Main Transformer Fire (Section 4OA3.1)

A-2

Attachment

LIST OF DOCUMENTS REVIEWED

Section 1R02: Evaluation of Changes, Tests, or Experiments

Power Uprate Modifications

TM 2003-022

Vibration Monitoring Equipment Installation on MS [Main Steam] & FW

[Feedwater] Piping

MM 2003-015

Reactor Feed Pump Suction Pressure Trip

MM 2003-016

Reactor Recirculation System Runback

MM 2003-026

AST [Alternate Source Term] Component Modification (OG-779

Installation)

MM 2003-028

APRM Flow Control Trip Reference Card Replacement

MM 2003-039

NSSS [Nuclear Steam Supply System]/BOP [Balance of Plant]

Instrumentation Upgrades

MM 2003-054

381 Line Overload Relay Setting

VYDC 2003-013

Installation of Additional Main Steam Safety Valve

Section 1R08: Inservice Inspection

Procedures

ENN-NDE 9.29, Rev 0 for UT of structural overlay (weld N5A)

PDI-UT-8, Rev B. Generic Procedure for UT of Weld Overlaid Austenitic Pipe Welds

ISI - 254, Rev 5, for remote ISI of RPV Welds

NE 8048, Rev 1 - In Vessel Visual Inspection

Drawings

ISI-PPV-103, Rev 3. Reactor Vessel

ISI-SLC-Part 4, Rev 3. SLC Piping ISO

D-7983-621 Rev G. UT/ET clad crack calibration block

6D30047, Rev 0, Wesdyne Calibration Standard PDI-01

Miscellaneous Reports

QA (Quality Assurance) Audit Report AR-2003-22b&c, dated 11/13/2003

GE (General Electric) RICSIL No. 050 of 4/23/1990, and GE SIL NO. 539, dated 11/5/1991

GE Reports INR-VYR24-04-01R2, 02R2, 03, & 04R1 on Steam Dryer Visual Indications

GE Nuclear Engineering (GENE) 0000-0028-0130-01, Revision 3, dated April 2004 on Steam

Dryer Unit End Plate Indications - Vermont Yankee R24

GENE-0000-0028-0130-02, Revision 3, dated April 2004 on Steam Dryer Drain Channel

Indications - Vermont Yankee R24

Section 1R17: Permanent Plant Modifications

Power Uprate Modifications

A-3

Attachment

MM 2003-015

Reactor Feed Pump Suction Pressure Trip

MM 2003-016

Reactor Recirculation System Runback

MM 2003-026

AST Component Modification (OG-779 Installation)

MM 2003-028

APRM Flow Control Trip Reference Card Replacement

MM 2003-039

NSSS/BOP Instrumentation Upgrades

MM 2003-054

381 Line Overload Relay Setting

Calculations

Vermont Yankee Calculation (VYC) 0693A Rev. 2 APRM Neutron Monitoring Trip Loops

VYC-2269 Rev. 0

Feedwater and Condensate Hydraulic Model Analysis

VYC-2309 Rev. 0

Steam Drain Line MS-189-D3 Check Valve Addition

License Amendment Documents

BVY 03-23

License Amendment Proposal for ARTS/MELLLA

BVY 03-39

Technical Specification Proposed Change # 257 (ARTS/MELLLA)

GE-NE-0000-0020

Entergy Nuclear Operations Incorporated Vermont Yankee Nuclear

Power

GE-NE-1500-0001

Station MELLLA+ Transient Analysis

NEDO-33090

Safety Analysis Report for Vermont Yankee Nuclear Power Station

Constant Pressure Power Uprate

NRC NRR Safety Evaluation for License Amendment No. 219 to DPR-28

Specifications/Procedures

AP 5226 Rev. 5

Calibration of Switchyard Breaker Failure Relays

VYSP-FS-074

Specifications for Safety Valves

VY IPE Vol 2

Individual Plant Examination for SRV/SV Reclosure

Section 4OA2.1: Routine Review of Problem Identification and Resolution

Condition Reports

2002-2581

RBCCW pumps failed to restart within time limit during ECCS [emergency core

isolation cooling] test

2002-2584

ECCS test data was accepted as satisfactory when some data was outside of

acceptance criteria

2003-1509

The C RHRSW pump cooling water supply solenoid valve failed to open as

required on pump start

2003-2321

No indicated cooling flow upon C RHRSW pump start

2004-0700

While troubleshooting a 4KV breaker on Bus-2-7, the breaker driving pawl broke

  • 2004-0840

Incorrect status of Decay Heat Removal was logged on the Critical Outage

Systems Status Form

  • 2004-0845

NRC resident question on RHR procedure wording

2004-0879

HPCI V23-845 failed IST testing

2004-0892

Water level in the reactor cavity exceeds limits during cavity floodup

A-4

Attachment

  • 2004-0897

Incorrect start dates used in ORAM-Sentinel for alternate DHR capability

determinations

2004-0918

Adverse trend - main steam isolation valve Appendix J test failures

2004-0942

HPCI V23-846 failed IST testing

2004-0955

As-found condition of V2-80 included a galled stem

2004-0968

Unsuccessful decon of diver

2004-0981

An observation was made from below vessel that a piece of control rod drive

housing support (shoot-out steel) was missing

2004-0986

Instructions for RWP not adhered to

2004-0998

RHR-46A allowed to overflow while working on the valve

2004-1005

B RHR pump trip during restart due to no suction path

2004-1017

V2-13-3 failed Appendix J local leak rate test

2004-1058

Flow noise from RO-10-105C, C RHR pump discharge orifice

2004-1091

Rad survey maps indicate need to perform alpha survey

2004-1117

Flow noise from C RHR pump discharge orifice

2004-1160

ASME rejectable indication on SLC weld

2004-1190

Weld electrodeoven left unlocked and unattended

  • 2004-1339

Two fuel segments could not be confirmed in storage container

2004-1409

A RBCCW did not start within the allowed ECCS start time

2004-1426

ECCS test exceptions

2004-1428

Reactor water clean up pump started with no suction path

2004-1548

P-8-1A leaking oil from upper bearing reservoir area

2004-1653

Excessive overtime approved without documentation

2004-1665

Potentially non-conservative scram setpoint values

  • 2004-1916
  1. 2 fan room has inadequate hose stream coverage due to modification to fan

room door

  • 2004-1928

Slight leakage on B SBGT demister loop seal piping union

2004-1989

Generator Ground alarm came in

2004-2015

Reactor Scram

2004-2017

Notification of Unusual Event (NOUE) declared due to plant fire and automatic reactor scram

2004-2019

Main transformer fire

  • 2004-2022

Discrepancy in post scram rod position indication

  • 2004-2023

Torus-to-drywell vacuum breaker indicating lights and alarm indicate breakers

may have cycled during the scram/transformer trip

  • 2004-2045

Repeat of P-8-1A leaking oil from upper bearing reservoir area

2004-2074

Failure to make timely notification of States upon declaration of unusual event on

June 18, 2004

  • Inspector-identified issues.

Section 4OA5.1: Temporary Instruction (TI) 2515/156, Offsite Power System Operational

Readiness.

Procedures

A-5

Attachment

Vermont Yankee Operating Procedure Form (VYOPF) 0150.03, CRO [Control Room Operator]

Round Sheet

AP 0172, Work Schedule Risk Management - On Line

ISO New England Master/Satellite Procedure #1, Nuclear Plant Transmission Operations,

Revision 0

ISO New England Master/Satellite Procedure #2, Abnormal Conditions Alert, Revision Dated

11/19/01

Licensee Event Reports (LERs)

Vermont Yankee Nuclear Power Station LER 87-008-00, Loss of Normal Power During

Shutdown Due to Routing All Off-Site Power Sources Through One Breaker

Vermont Yankee Nuclear Power Station LER 84-022-00, Diesel Generator Lockout Trip of

Both Generators

Maintenance Rule Documents

NRC Maintenance Rule Program Website Frequently Asked Questions (FAQs)

Vermont Yankee 10CFR50.65 NRC Maintenance Rule SSC Basis Document, 345K Volts AC

Electrical (345KV)

Vermont Yankee 10CFR50.65 NRC Maintenance Rule SSC Basis Document, 115K Volts AC

Electrical (115KV)

Operational Experience Documents

JA Fitzpatrick Operational Experience (OE) 16822, Reactor Scram due to Grid Instability

Significant Operating Experience Report (SOER) 9901, Loss of Grid

Miscellaneous Documents

Control room operator logs dated 8/17/87

VYC-1088, Vermont Yankee 4160/480 Volt Short Circuit/Voltage Study, Revision 3

A-6

Attachment

LIST OF ACRONYMS

AC

Alternating Current

ADAMS

Automated Document Access Management System

ALARA

As Low As Is Reasonably Achievable

AP

Vermont Yankee Administrative Procedure

APRMs

Average Power Range Monitors

ASME

American Society of Mechanical Engineers

CFR

Code of Federal Regulations

CR

Condition Report

CRO

Control Room Operator

CS

Core Spray

CY

Calendar Year

DBD

Design Basis Document

DHR

Decay Heat Removal

DOST

Diesel Oil Storage Tank

DP

Vermont Yankee Department Procedure

EALs

Emergency Action Levels

ECCS

Emergency Core Cooling System

EDGs

Emergency Diesel Generators

ET

Eddy Current Testing

EOP

Emergency Operating Procedure

ER

Event Report

FAQ

Frequently Asked Question

FW

Main Feedwater System

GE

General Electric

GENE

General Electric Nuclear Engineering

HPCI

High Pressure Coolant Injection

IMC

Inspection Manual Chapter

IPEEE

Individual Plant Examination External Events

IR

Inspection Report

ISI

Inservice Inspection

IST

Inservice Testing

KV

Kilovolt

LER

Licensee Event Report

LLRT

Local Leakage Rate Testing

MM

Minor Modification

MS

Main Steam System

NCV

Non-Cited Violation

NDE

Nondestructive Examination

NEI

Nuclear Engineering Institute

NOUE

Notice of Unusual Event

NRC

Nuclear Regulatory Commission

NRR

NRC Office of Nuclear Reactor Regulation

OE

Operating Experience

ON

Vermont Yankee Off-Normal Procedure

OP

Vermont Yankee Operating Procedure

A-7

Attachment

PI

Performance Indicator

PMT

Post Maintenance Testing

PSB

Public Service Board

QA

Quality Assurance

RCS

Reactor Coolant System

RCIC

Reactor Core Isolation Cooling

RFO

Refueling Outage

RHR

Residual Heat Removal

RHRSW

Residual Heat Removal Service Water

RPS

Reactor Protection System

RWP

Radiation Work Permit

SBGT

Standby Gas Treatment

SDC

Shutdown Cooling

SDP

Significance Determination Process

SEG

Simulator Evaluation Guide

SEN

Significant Event Notification

SFP

Spent Fuel Pool

SLC

Standby Liquid Control

SOER

Significant Operating Experience Report

SSC

Structures, Systems and Components

STP

Special Test Procedure

SW

Service Water

TI

Temporary Instruction

TM

Temporary Modification

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

UT

Ultrasonic Testing

VT

Visual Examination Testing

VY

Vermont Yankee

VYC

Vermont Yankee Calculation

VYDC

Vermont Yankee Design Calculation

VYOPF

Vermont Yankee Operating Procedure Form