ML030990094

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DC Cook, Unit 2, Issuance of Amendment No. 259, Increasing the Licensed Reactor Core Power Level by 1.66% from 3411 Megawatts Thermal (Mwt) to 3466 Mwt
ML030990094
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 05/02/2003
From: Stang J
NRC/NRR/DLPM/LPD3
To: Bakken A
Indiana & Michigan Electric Co
Stang J
References
TAC MB6751
Download: ML030990094 (6)


Text

May 2, 2003 Mr. A. Christopher Bakken III, Senior Vice President and Chief Nuclear Officer Indiana Michigan Power Company Nuclear Generation Group 500 Circle Drive Buchanan, MI 49107

SUBJECT:

DONALD C. COOK NUCLEAR PLANT, UNIT 2 - ISSUANCE OF AMENDMENT REGARDING MEASUREMENT UNCERTAINTY POWER UPRATE (TAC NO. MB6751)

Dear Mr. Bakken:

The U.S. Nuclear Regulatory Commission (NRC) has issued the enclosed Amendment No. 259 to Facility Operating License No. DPR-74 for the Donald C. Cook Nuclear Plant, Unit 2. The amendment consists of changes to the Technical Specifications in response to your application dated November 15, 2002, as supplemented February 24 and April 25, 2003.

The amendment increases the licensed reactor core power level by 1.66 percent from 3411 megawatts thermal (MWt) to 3468 MWt. The power level increase is considered a measurement uncertainty recapture power uprate.

By letter dated April 18, 2003, we issued a draft version of the enclosed safety evaluation (SE) and requested that you review it to verify that factual information is accurate and complete. By your April 25, 2003, supplemental letter, you provided comments on the draft SE. We have evaluated your comments and have incorporated them as appropriate. We note that your comments did not change our findings or conclusions discussed in the draft SE.

A copy of our related SE is enclosed. A Notice of Issuance will be included in the Commissions next biweekly Federal Register notice.

Sincerely,

/RA/

John F. Stang, Senior Project Manager, Section 1 Project Directorate III Division of Licensing Project Management Office of Nuclear Reactor Regulation Docket No. 50-316

Enclosures:

1. Amendment No. 259 to DPR-74
2. Safety Evaluation cc w/encls: See next page

ML030990094 (Cover Letter and Amendment)

ADAMS Accession No. ML031260667 (License and TS Pages)

ADAMS Accession No. ML030990129 (Safety Evaluation)

ADAMS Accession No. ML030990132 (Package)

Donald C. Cook Nuclear Plant, Units 1 and 2 cc:

Regional Administrator, Region III U.S. Nuclear Regulatory Commission 801 Warrenville Road Lisle, IL 60532-4351 Attorney General Department of Attorney General 525 West Ottawa Street Lansing, MI 48913 Township Supervisor Lake Township Hall P.O. Box 818 Bridgman, MI 49106 U.S. Nuclear Regulatory Commission Resident Inspectors Office 7700 Red Arrow Highway Stevensville, MI 49127 David W. Jenkins, Esquire Indiana Michigan Power Company One Cook Place Bridgman, MI 49106 Mayor, City of Bridgman P.O. Box 366 Bridgman, MI 49106 Special Assistant to the Governor Room 1 - State Capitol Lansing, MI 48909 Drinking Water and Radiological Project Division Michigan Department of Environmental Quality 3423 N. Martin Luther King Jr. Blvd.

P. O. Box 30630, CPH Mailroom Lansing, MI 48909-8130 Scot A. Greenlee Director, Nuclear Technical Services Indiana Michigan Power Company Nuclear Generation Group 500 Circle Drive Buchanan, MI 49107 David A. Lochbaum Union of Concerned Scientists 1616 P Street NW, Suite 310 Washington, DC 20036-1495 Michael J. Finissi Plant Manager Indiana Michigan Power Company Nuclear Generation Group One Cook Place Bridgman, MI 49106 Joseph E. Pollock Site Vice President Indiana Michigan Power Company Nuclear Generation Group One Cook Place Bridgman, MI 49106

INDIANA MICHIGAN POWER COMPANY DOCKET NO. 50-316 DONALD C. COOK NUCLEAR PLANT, UNIT 2 AMENDMENT TO FACILITY OPERATING LICENSE Amendment No. 259 License No. DPR-74 1.

The U.S. Nuclear Regulatory Commission (the Commission) has found that:

A.

The application for amendment by Indiana Michigan Power Company (the licensee) dated November 15, 2002, as supplemented February 24 and April 25, 2003, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act), and the Commissions rules and regulations set forth in 10 CFR Chapter I; B.

The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Commission; C.

There is reasonable assurance (i) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commissions regulations; D.

The issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public; and E.

The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commissions regulations and all applicable requirements have been satisfied.

2.

Accordingly, the license is amended by changes to the Technical Specifications as indicated in the attachment to this license amendment, and paragraph 2.C.(2) of Facility Operating License No. DPR-74 is hereby amended to read as follows:

(2)

Technical Specifications The Technical Specifications contained in Appendices A and B, as revised through Amendment No. 259, are hereby incorporated in the license. The licensee shall operate the facility in accordance with the Technical Specifications.

In addition, the license is amended to revise paragraph 2.C.(1) to reflect the increase in the reactor core power level. Paragraph 2.C.(1) is hereby amended to read as follows:

The licensee is authorized to operate the Donald C. Cook Nuclear Plant, Unit No. 2, at steady state reactor core power levels not to exceed 3468 megawatts (thermal).

3.

This license amendment is effective as of the date of issuance and shall be implemented within 90 days of the date of issuance. Prior to implementation of the license amendment, the licensee shall:

A.

Install a leading edge flowmeter CheckPlus system. The design change for the installation will include instrumentation rescaling, Updated Final Safety Analysis Report (UFSAR) revision, maintenance and operational procedure revisions, training, monitoring iso-phase bus duct temperature, and implementation of the LEFM CheckPlus system out-of-service administrative technical requirements, as described in the licensees November 15, 2002, application. The UFSAR revision shall be reflected in the next update of the UFSAR submitted to the NRC pursuant to 10 CFR 50.71(e)

B.

Complete a formal reload safety evaluation, as described in the licensees November 15, 2002, application, and evaluated in the associated safety evaluation by the Office of Nuclear Reactor Regulation, dated May 2, 2003. The evaluation shall be reflected in the next update of the UFSAR submitted to the NRC pursuant to 10 CFR 50.71(e).

C.

Complete an analysis of the steam dump valves flow capacity at the uprated power level and based on this analysis, implement any changes/adjustments necessary to ensure the valves have sufficient capacity prior to implementing the 1.66-percent power uprate. The analysis and any changes/adjustments to the steam dump valves shall be reflected in the next update of the UFSAR submitted to the NRC pursuant to 10 CFR 50.71(e).

FOR THE NUCLEAR REGULATORY COMMISSION

/RA/

Ledyard B. Marsh, Acting Director Division of Licensing Project Management Office of Nuclear Reactor Regulation

Attachment:

Changes to the Operating License and Technical Specifications Date of Issuance: May 2, 2003

ATTACHMENT TO LICENSE AMENDMENT NO. 259 FACILITY OPERATING LICENSE NO. DPR-74 DOCKET NO. 50-316 Replace the following page of Facility Operating License No. DPR-74 with the attached revised page. The revised page is identified by amendment number and contains marginal lines indicating the areas of change.

REMOVE INSERT 3

3 Replace the following pages of the Appendix A Technical Specifications with the attached revised pages. The revised pages are identified by amendment number and contain marginal lines indicating the areas of change.

REMOVE INSERT 1-1 1-1 3/4 5-3 3/4 5-3 3/4 7-2 3/4 7-2