05000272/LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl

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Forwards LER 82-012/03L-0.Detailed Event Analysis Encl
ML20050C289
Person / Time
Site: Salem PSEG icon.png
Issue date: 03/24/1982
From: Midura H
Public Service Enterprise Group
To: Haynes R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20050C290 List:
References
NUDOCS 8204080377
Download: ML20050C289 (3)


LER-1982-012, Forwards LER 82-012/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
2721982012R00 - NRC Website

text

'

O PSIEG Pi;bhc Service Electric and Gas Comp 3ny P.O. Box E Hancocks Bridge, New Jersey 08038 Salern Generating Station M

982 na s.'

4 Mr.

R. C. Ilaynes

- 3' OPR 7

} M 5 Mt Cp:n cwa 1932 3 Regional Administrator USNRC Region 1 A

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631 Park Avenue King of Prussia, Pennsylvania 19406 3

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Dear Mr. Ilaynes:

LICENSE NO. DPR-70 DOCKET NO. 50-272

REPORTABLE OCCURRENCE 82-12/03L Pursuant to the requirements of Salem Generating Station Unit No. 1, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable occurrence 82-12/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

/a/ j/

ocV 11. J. Midura General Manager -

Salem Operations FD:al.

CC:

Distribution-8204000377 920324 PDR ADOCK 05000272

.O PDR The Energy Peoplo

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a, vd I n si

Report Number:

82-12/03L Report Date:

03-24-82 Occurrence Date:

02-23-82 Facility:

Salem Generating Station, Unit 1 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

No. IB Diesel Generator - Inoperable.

This report was initiated by Incident Report 82-041.

CONDITIONS PRIOR TO OCCURRENCE:

Mode 6 - Rx Power 0% - Unit Load 0 MWe DESCRIPTION OF OCCURRENCE:

On-February 23, 1982, while performing his rounds, an operator discovered that No.1B Diesel Generator cubicle contained a significant amount of chromated water on the floor.

An elec-trical conduit containing leads to the pre-lubrication pump and heater was filled with the water.

Investigation revealed that the right side jacket water heater was leaking at it's connection to the diesel.

At 0225 hours0.0026 days <br />0.0625 hours <br />3.720238e-4 weeks <br />8.56125e-5 months <br /> No. 1B Diesel was declared inoperable, and since No. 1C Diesel was already tagged out, Action Statements 3.8.1.2 and 3.8.2.2 were entered.

This occurrence constituted operation in a degraded mode in accordance with Technical Specification 6.9.1.9.b..

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

^

The right side jacket water heater was leaking.

Design Change Request.(DCR) ISC-0086 has been issued to replace the heaters with a variety utilizing a more corrosion resistant sheath to retard corrosive action, and prevent filling the conduit with chromated water.

ANALYSIS OF OCCURRENCE:

Technical Specification 3.8.1.2 requires:

With less than the above minimum required A.C. electrical power sources operable, suspend all operations involving core-alterations or positive reactivity changes until the minimum required A.C. electrical power sources are restored

- to operable status.

~

~

LER 82-12/03L,

Technical Specification 3.8.2.2.

requires:

With less than_the above complement of A.C. busses operable and energized,. establish containment integrity within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />.

CORRECTIVE ACTION

All operations: involving core alterations or positive reactivity changes were suspended immediately.

Containment integrity was established at 1020 hours0.0118 days <br />0.283 hours <br />0.00169 weeks <br />3.8811e-4 months <br />, February 23.

Both_ jacket water heaters _ were replaced as per DCR ISC-0086.

The prelubrication pump and motor were replaced.

The conduit was flushed out and~

dried.- No.1B Diesel was tested satisfactorily and declared operable.

At 0215 hours0.00249 days <br />0.0597 hours <br />3.554894e-4 weeks <br />8.18075e-5 months <br />, February 24, 1982 Action Statments 3.8.1.2'and 3.8.2.2. were terminated.

FAILURE DATA:

- Jacket Water Heaters Alco Part No. 72-82990-090 Prelubrication Pump
- Viking Model IIJ-475M Prelubrication Pump Motor General Electric,'3 H.P.

No. SKl82J254C Prepared By F.

Dickey

/*

'd General-Manager -

SORC Mocting No.

82-32 t